ML18011B059
| ML18011B059 | |
| Person / Time | |
|---|---|
| Site: | Harris |
| Issue date: | 11/03/1995 |
| From: | Darrell Roberts, Shymlock M NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML18011B056 | List: |
| References | |
| 50-400-95-15, NUDOCS 9511160262 | |
| Download: ML18011B059 (34) | |
See also: IR 05000400/1995015
Text
UNITED STATES
NUCLEAR REGULATORY COMMISSION
REGION II
101 MARIETASTREET, N.W., SUITE 2900
ATLANTA,GEORGIA 303234199
Report No.:
50-400/95-15
Licensee:
Carolina
Power 5 Light Company
P. 0.
Box 1551
Raleigh,
NC 27602
Docket No.:
50-400
Facility Name:
Harris
1
Inspection
Conducted:
September
3 - October 7,
1995
License No.:
Inspecto
~
~
D.
Ro erts,
Act)ng Sen>or
es1
ent
nspector
Other Inspector:
S. Elrod, Senior Resident
Inspector
Approved by:
. Symoc,
C1e
Reactor Projects
Branch
4
Division of Reactor Projects
Zls sW
ate
igne
ate
igne
SUMMARY
Scope:
This routine inspection
was conducted
in the areas of operations,
maintenance,
surveillance,
engineering,
plant support,
review of licensee
event reports,
and licensee
action
on previous inspection
items.
Numerous facility tours
were conducted
and facility operations
observed.
Results:
Plant
0 erations
Midloop operations,
refueling activities,
and control
room response
to a
smoking breaker cubicle were good.
Contractor performance
during core
manipulations
was good.
Personnel
and process
errors
were noted in other
areas
which warranted
increased
licensee
management
attention,
paragraph
3.b.
An inadequate
procedure
resulted
in an unplanned
actuation of the turbine
driven auxiliary feedwater
pump
and
an
LER, paragraph 3.f.(1).
The inspectors
identified one violation in the Operations
area which was significant because
it involved
a situation where operators
were not aware of the inoperable
status of the "B" CSIP,
causing
them to place it in service
on September
2
without it being properly tested,
paragraph 3.a.(l).
95iiih0262 95ii03
ADOCK 05000400
Q
Maintenance
Overall, maintenance
and surveillance activities were conducted well during
the outage.
However,
one violation was caused
by an inadequate
procedure
which led to an unplanned partial safety injection, paragraph,5.c.
En ineerin
Overall, engineering activities were performed well, especially considering
the many engineering
challenges
that were presented
during the refueling
outage.
The inspectors
identified no violations or deviations
in the
engineering
area.
Plant
Su
ort
Licensee
performance
in the radiological controls
area
was
good during the
refueling outage,
paragraph
6.b.
PNSC meetings
had good safety focus,
paragraph 6.f.
REPORT DETAILS
PERSONS
CONTACTED
Licensee
Employees
D. Batton, Superintendent,
On-Line Scheduling
D. Braund,
Manager,
Security
J. Collins, Manager,
Training
- J. Dobbs,
Manager,
Outage
and Scheduling
- J. Donahue,
General
Manager,
Harris Plant
R. Duncan,
Superintendent,
Mechanical
Systems
- W. Gautier,
Manager,
Maintenance
H.
Hamby,
Manager,
Regulatory
Compliance
- H. Hill, Manager,
Nuclear Assessment
D. HcCarthy, Superintendent,
Outage
Management
- R. Prunty,
Manager,
Licensing
and Regulatory
Programs
- W. Robinson,
Vice President,
Harris Plant
- G. Rolfson,
Manager,
Harris Engineering
Support Services
S. Sewell,
Superintendent,
Design Control
- T. Walt, Manager,
Regulatory Affairs
- B. White, Manager,
Environmental
and Radiation Control
- A. Williams, Manager,
Operations
Other licensee
employees
contacted
included:
office, operations,
engineering,
maintenance,
chemistry/radiation control,
and corporate
personnel.
NRC Personnel
C, Bajwa,
Systems
Engineer,
Office of Nuclear Reactor Regulation
(NRR)
- S. Elrod, Senior Resident
Inspector,
Harris Plant
- C. Lui, Risk Assessment
'Engineer,
Office of Nuclear Regulatory
Research
- D. Roberts,
Resident
Inspector,
Harris Plant
L. Whitney, Project Manager,
F. Wright, Senior Radiation Specialist,
Region II
- Attended exit interview
and initialisms used
throughout this report are listed in the
last paragraph.
PLANT STATUS AND ACTIVITIES
'a
0
Operating Status of the Plant Over the Inspection
Period.
The plant
began
the inspection
period being cooled
down in
preparation for refueling.
At the time, the plant was in Hot
Shutdown
(Mode 4) with RCS temperature
and pressure
about
325 'F
and 350 psig, respectively.
Operators
continued to cool
and
depressurize
the plant, entering
Cold Shutdown
(Mode 5)
on
September
3.
The plant entered
Refueling
(Mode 6)
on September
9.
Fuel
was completely offloaded from the reactor vessel
from
September
12 to 15.
The plant re-entered
Mode
6 on
September
26 when the first fuel bundle
was reloaded into the
0'
reactor
vessels
Core reload
was complete
on September
28.
The
plant entered
Mode
5 on October
2 when the reactor vessel
head
studs
were fully tensioned.
The plant
commenced
the post-outage
heatup
on October
7, entering
Mode
4 that morning
and
Mode
3 that
afternoon.
The plant ended the inspection period in Mode 3 with
RCS heatup
in progress
and
RCS temperature
and pressure
approaching
normal operating conditions.
b.
Other
NRC Inspections
or Meetings at the Site.
F. Wright, Senior Radiation Specialist,
NRC RII, was
on site from
September
18-22 conducting
an inspection
in the area of
radiological control
and protection.
The inspector
conducted
an
exit meeting
on September
22
and his findings were documented
in
IR 400/95-14.
C. Lui, Risk Assessment
Engineer,
NRC Office of Nuclear Regulatory
Research,
was
on site from September
11 - October
6 observing
outage activities.
C.
Bajwa and
L. Whitney, both of the
NRC Office of Nuclear Reactor
Regulation,
were
on site
on October
5 and
6 viewing plant fire
protection modifications
and studying post-fire safe
shutdown
procedures.
The
NRC representatives
were accompanied
by Messrs.
T. Storey
and
K. Sullivan,
both
NRC contractors,
and Mr. N.
Berkoff,
a U.S.
Department of State contract interpreter.
Also
accompanying
the
NRC staffmembers
were fourteen foreign visitors
representing
the Russian
Federation
regulatory
body,
Russian
industrial fire protection government ministry, Russian
power
reactor plant operating organization,
Ukrainian regulatory
body,
Ukrainian industrial fire protection/fire fighting and research
organizations,
and
Czech Republic
and Hungarian regulatory bodies.
OPERATIONS
a
~
Plant Operations
(71707)
(1)
Shift Logs
and Facility Records
The inspector
reviewed records
and discussed
various entries
with operations
personnel
to verify compliance with the
TS
and the licensee's
administrative
procedures.
In addition,
the inspector
independently verified clearance
order
tagouts.
0 eration in Mode
4 with Potentiall
No 0 erable
CSIPs
With the plant in Node
4 on September
2, the inspector
reviewed the Shift Supervisor's
logbook and discovered that
operators
had declared
and placed in service the
"B" charging/safety
injection
pump
(CSIP) without properly
testing it.
The "A" and
"C" CSIPs
were removed
from service
and declared
inoperable to satisfy
LTOP requirements
contained
in TS 3. 1.2. 1 (Boration Systems
Flowpath)
and
(ECCS Subsystems)
with RCS temperature
less
than
325
'F.
The "C" pump's electrical
breaker
was racked out and
the "A" pump's
manual
discharge
valve
had. been
locked closed
to prevent either
pump from injecting with the plant in a
pressurized,
low temperature
condition.
Prior to this
configuration
and for much of the previous operating cycle,
the
"A" and
"C" pumps
had
been in service satisfying
Node 1-
3 TS requirements.
The following paragraphs
discuss
how the
"B" pump should not have
been declared
on September
2 since it had not been properly tested prior to placing it
in service.
~Back round
Each
CSIP has
a miniflow system that ensures
a vendor-
recommended
minimum flowrate of 60
GPN for pump protection.
The "8"- CSIP had
been out of service
and inoperable for much
of the previous operating cycle due to
a failed check valve
(1CS-193)
in its miniflow system.
A stuck disk caused
the
valve to experience significant backflow leakage
over the
cycle requiring that the "B" pump not be placed in service
concurrent with the
"A" pump.
The backflow leakage
did not
affect operability of the
"B" pump,
which only required that
the check valve pass
forward flow.
However,
a postulated
"B" train electrical failure would take out the "8" pump,
and the undesirable
check valve leak path could potentially
divert enough
"A" pump flow during
a
LOCA, thus preventing
the "A" pump from performing its safety function.
Because
of the backflow leakage
problems,
in late July
licensee
personnel
replaced
the check valve (a 2-inch
T-style globe check valve with a resilient seating
surface)
with another T-style valve minus the soft seat.
Later,
on
August 2, the inspector
observed
the newly installed check
valve fail
a forward flow test,
passing
approximately
28
gpm, vice 60 gpm.
The failure was caused
by a sticking disk
inside the valve.
After this failure,
between
August
2 and
September
2, operators
maintained
compliance with Node 1-3
Technical Specifications
by using the
"C" pump to replace
the
"B" pump
and isolating the "B" pump's miniflow leak path
from the "A" pump.
The inspector,
recalling that successful
completion of the
forward flow test
was
a prerequisite for "B" pump
operability, questioned its operability on September
2.
This information was indicated to the control
room,
The
control
room operators
were unaware of the earlier
forward flow failure.
After researching
the previous
month's test records
and the reactor operator's
logbook
entry for August 2, the operators
determined that the "8"
pump had
indeed not been successfully
tested prior to
placing it in service
on September
2.
At the time of this
discovery,
RCS temperature
was less
than
325 'F.
Operators
immediately corrected
the situation
by raising
temperature
above
325 'F to ensure
compliance with LTOP
requirements,
opening the "A" pump's discharge
isolation
valve,
and placing that
pump in service.
After securing
the
"8" pump
and racking out its breaker,'perators
continued
the plant cooldown to Mode 5,
Root Cause
Operators
improperly placed the "8" pump in service
because
they were
unaware of its inoperable status
since August 2,
Further review determined
the root cause
to be inadequate
Equipment
Records
(EIRs) for both valve
and the "8" CSIP.
The EIRs did not reference
the valve's
forward flow test failure.
EIRs were
used to document
equipment,
failed surveillance tests,
and
associated
retest
requirements.
These
forms were relied
upon
by operators
to ensure that
TS
LCOs were complied with
when manipulating or testing plant equipment.
'he
EIRs associated
with the "8" CSIP
and valve
were
initiated in July because
of the previous backflow test
failure, but were not updated
by the
SCO on August
2 when
the newly replaced
valve failed the forward flow test.
Responsible
plant personnel
incorrectly assumed
on August
2
that because
the valve was already inoperable prior to the
forward flow test,
the
EIRs generated
in July were properly
annotated
with retest
requirements.
Since "8" pump miniflow
check valve backleakage
only affected
"A" pump operability,
the "8" pump
EIR only referenced
that the pump's breaker
had
to be racked
in to make it operable.
Likewise, the only
retest
requirement
referenced
on the
EIR was its
backflow leak test.
Successful
completion of this test
would be required prior to unisolating the valve from the
"A" pump to maintain that pump's operability.
On September
2,
because
of the incomplete information in the
EIRs, operators
placed the "8" CSIP in service to support
an
upcoming
18-month surveillance test without forward flow
testing the miniflow check valve,
and
made the other
pumps
The plant was operated
in this condition for
approximately
seven
hours before the inspector discovered
it.
During that time, operators
were cooling down the
in accordance
with operating
procedures,
thereby
adding
positive reactivity to the core with one degraded
CSIP
functional.
Operations
Management
Manual procedure
OHH-014,
Rev.
4,
Operation of the Work Control Center,
Step 5.3.6 required
that the
SCO annotate all applicable
EIRs when equipment
failed surveillance testing or portions of the test which
were not completed.
Procedure
OHH-014 further required that
the
SCO do this by entering all pertinent information in the
Remarks section of the EIR, which was Attachment
4 to the
'rocedure.
Procedure
OMM-007, Rev.
4, Operations
Surveillance,
Periodic
and Reliability Tests,
required that
the Shift Supervisor
ensure that
an
EIR was completed
when
an
OST failed to meet its acceptance
criteria.
The failure
to complete the "B" CSIP
and valve
EIRs with forward
flow test information resulted
in the plant operating in
Mode
4 for over
7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> with one degraded
CSIP.
The failure
to follow procedures
OMH-007 and
OMH-014 was contrary to the
requirements
of TS 6.8. Ia and Regulatory
Guide 1.33,
Rev.
2,
Appendix A which required procedures
for equipment control.
This is identified as Violation 400/95-15-01,
Failure to
Properly Annotate Surveillance
Test Requirement for an
CSIP.
Safet
Si nificance
Although this violation resulted
in the
"B" CSIP being
placed in service without testing its miniflow system,
the
safety consequences
were minimal.
At the time of the
discovery,
the inspector verified that at least
a 60
gpm
flowrate existed via the normal charging/seal
injection
flowpath.
Additionally, the licensee initiated
ESR 9500752
to show that the
"B" pump never operated
below its minimum
flow limit and that it could have performed its safety
function with the plant in Mode
4 and
RCS pressure
reduced
to 350 psig.
The licensee's
evaluation is further discussed
in paragraph
5.a.4 of this report.
While the event's
safety
significance
was minor, the problem could have resulted
in a
substantial
safety hazard
under different plant operating
conditions
(Modes
1,
2 or 3).
Corrective Actions
To correct the valve problem,
the licensee
replaced
the T-
style globe check valve with a Y-type valve.
The
new valve
had
a disk arrangement
designed
to operate better under
higher system pressures.
The valve subsequently
passed
both
forward flow and backflow leakage tests.
To correct the
EIR
documentation
problem, operations
management
issued night
orders describing
the event
and discussing
the
need for more
attention to detail in documenting surveillance test
results.
The licensee
documented this event in LER 95-08 which is
closed in paragraph 3.f.(2) of this report.
The licensee
also reported
the check valve deficiency in accordance
with
The inspectors
found the logs
and other facility records to
be legibl'e
and well organized,
and to provide sufficient
information on plant status
and events.
The inspectors
found clearance
tagouts
to be properly implemented.
The
inspectors
identified one violation in this area.
(2)
Facility Tours
and Observations
Throughout the inspection period,
the inspectors
toured the
facility to observe activities in progress,
and attended
several
licensee
meetings
to observe
planning
and management
activities.
Inspectors
made
some of these
observations
during backshifts.
During these tours,
the inspectors
observed
monitoring
instrumentation
and equipment operation.
The inspectors
also verified that operating shift staffing met
TS
requirements
and that the licensee
was conducting control
room operations
in an orderly and professional
manner.
The
inspectors
additional,ly observed
several shift turnovers to
verify continuity of plant status,
operational
problems,
and
other pertinent plant information.
Licensee
performance
in
these
areas
was satisfactory.
The inspectors
identified no violations or deviations
in the
facility tours
and observations
area.
Effectiveness
of Licensee
Control in Identifying, Resolving,
and
Preventing
Problems
(40500)
Condition Reports
(CRs) were reviewed to verify that
TS were
complied with, corrective actions
and generic
items were
identified,
and items were reported
as required
by 10 CFR 50.73.
Several
CRs documenting
personnel
or process
errors
were generated
during the refueling outage.
While the numerous
CRs indicated
that the licensee's
threshold for documenting
nonconformances
was
relatively low,
some of these
CRs described
incidents that
warranted additional
management
attention in the area of work
performance
and clearances.
The following incidents
documented
in
CRs were noteworthy:
Operator error in conducting the Loss of Offsite Power/LOCA
sequencing
test resulted
in the "A" RHR pump starting twice
in 20 seconds,
as discussed
in paragraph
4.b.(2) of this
report.
Due to
a process error, operators
inadvertently placed
"A" and
"C" under clearance.
Per the licensee's
shutdown risk assessment,
the valves were
assumed
to be part
of a key safety function available during cold shutdown,,
maintaining the
as
a diverse
decay heat
removal
method.
When operators
realized the error, the "A" and
"C" SG
were returned to functional status.
Fortunately,
defense
in
depth
was not compromised
as the
RHR pumps were both
and in service at the time.
Upon installing an inappropriate
clearance,
operators
isolated
instrument air to the containment building, thereby
isolating the normal
CVCS letdown flowpath.
The clearance
also caused
discharge
isolation valve
to unexpectedly
close, essentially
removing
one train of
from service,
Fortunately,
RCS letdown was aligned to the
RHR system at the time which eliminated the potential for
unexpected
RCS heatup.
Operators
promptly restored
the
by placing the normal service water
system in service,
The above incidents,
including the inoperable
CSIP event discussed
in section 3.a.(1), all occurred during the first few days of the
outage.
While errors like these
were reduced
as the outage
continued,
other performance deficiencies
surfaced
(improperly
restored
clearances,
poor
FME controls) which warranted
increased
management
attention in this area.
Refueling Activities (71707)
The inspector
observed
fuel offload and reload activities in
accordance
with fuel handling procedures
FHP-014,
Rev.6,
Fuel
and
Insert Shuffle Sequence,
and
FHP-020,
Rev. 7/3, Refueling
Operations.
Fuel handling equipment,
including the refueling
bridge crane,
hoist,
and load cell
had
been properly tested,
inspected
and calibrated prior to fuel movement,
as required
by
plant procedures.
The fuel handling equipment
performed well
during the evolutions.
Operators
mairitained the refueling cavity
water level at
23 feet
above the reactor vessel
flange during fuel
movement.
The licensee's
FME program
was in effect, with areas
around
and
above the refueling cavity properly controlled
as
boundaries.
An
FME coordinator signed
people
and equipmeht in and
out of the
FME zone
as required
by plant procedures.
Potentially
loose articles
were properly tied off.
The inspector
observed
that the fuel movement
was directly supervised
by
a licensed
senior reactor operator,
as required
by TS 6.2.2d.
Licensee
and
'ontractor personnel
performed these
core manipulations
in
a
skilled and professional
manner.
Midloop Operations
(71707)
Due to continuing work in the steam generators,
the plant
had to
go into midloop operations after core reload during the weekend of
September
30.
The inspectors verified that midloop and reduced
inventory activities were conducted
in accordance
with
expectations
contained
in
"Loss of Decay
Heat Removal."
Specifically, the inspectors verified that
procedural
controls were in place
and certain
systems
were
available throughout the operation.
Additionally, the inspectors
ascertained
that operators
were trained
and pre-briefed
on the
evolution;
and were
aware of associated
risks.
Operators
received control
room training on midloop operations
just days prior to the evolution.
Additionally, pre-job briefings
were conducted for each
involved shift.
Procedures
covering the
evolution included General
Procedure
GP-08,
Draining the Reactor
Coolant System;
and
OMP-004, Control of Plant Activities During
Reduced
Inventory Conditions.
These
procedures
required at least
two independent
core exit temperature
indications,
two independent
reactor
vessel
water level indications,
and
two additional
means
of adding.,inventory to the
be available.
Containment closure
requirements
were conta'ined
in OST-1091,
Containment
Closure Test,
Weekly Interval;
and OST-1034,
Containment
Test,
Weekly.
The inspectors verified that all system availability and
containment closure requirements
were met prior to and during
reduced
inventory operations.
Additionally, only two of the three
had nozzle
dams installed,
so the reactor vessel
was adequately
vented.
The inspector
concluded that the licensee's
controls for midloop
operations
were adequate.
Additionally, operators
performed
draindown activities well.
Plant
Response
to .Fire Announcement
(71707)
The inspectors
observed
plant response
to
a perceived
switchgear
fire..
On September
29, during
a containment
spray actuation test
procedure,
an Asea
Brown Boveri Model
LK-16 breaker failed to trip
open
as required.
This breaker,
located
in non-safety related
switchgear cubicle
served
a containment pre-entry
purge
fan,
E-5B, which was
supposed
to trip on low flow following the
containment
spray actuation.
Personnel
observed
smoke
coming from
the breaker cubicle
and communicated this to the main control
room.
After control
room personnel
sounded
the plant fire alarm,
the shift supervisor
announced
the location of the "fire" and
requested fire brigade
response.
When the inspector arrived at
the switchgear,
there
was
no fire and personnel
had racked out the
breaker.
There
was
a burning smell
and personnel
explained that
there
had
been
no fire, but the trip coil in the breaker
had
overheated
and released
smoke into the area.
This had
been
a
recurring problem over the years with 480 volt LK-16 breaker trip
coils.
Over the last two refueling outages,
the licensee
replaced
all LK-16 safety-related
breakers
and frequently cycled non-safety
related
breakers
with a Siemens
model.
This breaker
was not
considered
a frequently cycled breaker
and
was not replaced.
The plant fire brigade
responded
to the control
room announcement
in a timely manner,
The inspector
concluded that the control
room's
prompt response
and cautious
actions regarding the
perceived "fire" was excellent.
Review of LERs (92700)
'(1)
(Open)
LER 95-007-00,
Inadvertent Start of the Turbine
Driven
AFW Pump/Unplanned
ESF Actuation and Identification
of an Additional Related Test Deficiency.
This
LER discussed
a procedural
deficiency that, during
an
"A" train safety
bus undervoltage
relay logic test,
caused
an ina'dvertent start of the turbine driven
AFW pump
and
resultant
feeding of the steam generators.
During the
investigation of the
pump actuation,
the licensee
discovered
another reportable
procedural
deficiency related to testing
of undervoltage
relays.
Both items were reported
on
LER
95-07
and are discussed
below.
On September
1, plant personnel
performed procedure
HST-E0034,
6.9KV Emergency
Bus,
1A-SA Under Voltage
(Loss of
Voltage)
Channel Calibration.
The plant was in Mode
1 at
approximately
75% reactor
power and the procedure
was
a post
maintenance
test following calibrations
on each of three
6.9kV bus
relays.
The procedure called
for depressing
a test push-button
which caused
actuation of
both the undervoltage
lockout relay
86UV and the test
lockout relay 86T.
The 86T test relay blocked signals
from
the
86UV relay
and its associated
relays except for a signal
from relay
86UVX to the
TDAFW pump steam
supply valve,
1HS-
70.
Since that signal
was not blocked,
and the logic for
opening the valve
on
a bus undervoltage
was satisfied,
the
valve stroked
open
and provided
steam to the Terry turbine.
During an investigation into the above event,
licensee
personnel
discovered
another
TDAFW pump testing deficiency
related to the
86UVX relay.
Specifically,
TS 4.3.2. 1 and
TS
Table 4.3-2 contained
monthly Trip Actuating Device
Operational
Test
(TADOT) requirements
applicable to both the
motor driven
AFW pumps
and the
TDAFW pump.
The motor driven
pump requirement
was covered
by procedure
OST-1124,
6.9kV
Emergency
Bus Undervoltage Trip Actuating Device Operational
Test Monthly Interval
Modes 1-2-3-4, which had personnel
visually verify that the
86UV relay rolled during testing.
Plant procedure writers incorrectly assumed
that the turbine
driven
pump was also covered
by visual observation of the
10
86UV relay,
and did not understand
that the associated
86UVX
relay was also in the starting circuit.
Thus, the monthly
test procedure
did not contain directions to verify
actuation of the
86UVX relay,
and the monthly TS requirement
was never covered.
Licensee
personnel
determined that the root cause of both
events
was procedural
error.
Related to the inadvertent
pump actuation,
plant surveillance
procedures
generally
contained
mode restrictions
and statements
cautioning
personnel
on plant conditions which may affect test
performance.
The bus undervoltage test procedure
HST-E0034
allowed the test to be performed in Hodes
1 through 6,
inclusive,
and contained
no precautions
describing
what
would happen if the test
was performed in Hodes
1 though
4
with steam available to the turbine.
The test
was normally
performed in Hodes
5 and
6 with no plant steam
such that
when valve IHS-70 opened,
the
TDAFW pump would not start.
Because of the procedural
omissions,
personnel
performing
the procedure
on September
1 were unaware of the potential
pump start.
The safety significance of both issues
was minimal.
There
were
no adverse
affects
on safe plant operation,
no
pump
damage,
and
no resultant inoperability of safety
systems
following the inadvertent
TDAFW pump start.
Operators
in
the control .room secured
AFW flow to the steam generators
in
a timely manner.
Although the
86UVX relay was never
verified on
a monthly basis
as required
by TS, its actuation
on bus undervoltage
was verified every
18 months
by
deenergizing
the safety
bus during the TS-required
operability tests.
The licensee's
corrective actions will include revising the
procedures
to correct the surveillance test deficiencies.
This
LER will remain
open pending licensee
completion
and
inspector review of corrective actions.
(Closed)
LER 95-008-00,
"B" Charging/Safety
Injection
Pump
was Returned to Service Prior to Required
Acceptance
Testing,
Resulting in Technical Specification Violation.
This inspector identified violation was discussed
in
paragraph 3.a.(l) of this report.
The
LER is closed
and the
licensee's
corrective actions will be tracked with Violation
400/95-15-01.
11
g.
Followup
Operations
(92901)
(Closed)
IFI 95-11-01,
guestionable
Position Indication for
Containment Isolation Valve 1SP-209.
The inspector consulted
NUREG-1482, Guidelines for Inservice
Testing at Nuclear
Power Plants,
to determine
the
need for
verifying both the
open
and closed positions for valves having
one
safety function.
In this case,
valve
gave dual
(mid-
position) indication in the control
room on Hay
11 when operators
took its control switch to the open position.
The valve in
question
was
a small
sealed
solenoid valve for which only remote
position indication was available.
The valve's safety function
was to close
on
a containment isolation signal.
Licensee
management
determined that,
since the closed position was never in
question,
the valve remained
from Hay
11 until the
valve's next inservice test
became
due.
At that time both the
open
and closed positions
would need verification for stroke
timing as required
by ASHE Section
XI Inservice Testing
Requirements,
and
implemented
by the licensee's
program procedure
ISI-203,
ASME Section
XI Pump
and Valve Program Plan.
From the review of NUREG-1482,
the inspector determined that
no
additional verification was required for the valve to remain
on or after Hay 11.
Stroke time testing
on June
12,
which included timing the valve stroke from fully open to fully
closed
(based
on control
room indication)
was adequate.
Further
valve operations
did not give the
same
dual position indication.
This item is closed.
Hidloop operations,
refueling activities,
and control
room response
to
a
smoking breaker cubicle were good.
Contractor performance
during core
manipulations
was good..
Personnel
and process
errors
were noted in
other areas
which warranted
increased
licensee
management
attention.
The inspectors
identified one violation in the Operations
area which was
significant because it involved
a situation where operators
were not
aware of the inoperable
status of the "B" CSIP,
causing
them to place it
in service
on September
2 prior to it being properly tested.
MAINTENANCE
Maintenance
Observation
(62703)
The inspector
observed
the maintenance
and reviewed the work
packages
for the following maintenance
activities to verify that
correct equipment
clearances
were in effect, work requests
were
issued,
and
TS requirements
were being followed.
12
WR/JO 95-ACAYI, Remove Reactor
Head Before Core Offload
Prior to fuel offload,
on September
11 the inspector
observed
personnel
removing the integrated
reactor vessel
head
and placing it on its storage
stand located
on the
refueling floor.
This evolution was performed in accordance
with procedure
CM-M0094, Integrated
Reactor
Vessel
Head
And
Upper Internals
Removal,
by both licensee
and contractor
personnel.
Personnel
were stationed
on the refueling
operating
deck
and at the refueling cavity floor ensuring
that the head lifted smoothly without snagging
guide studs,
the currently stuck stud,
or upper internals
components.
Once the
head
was
removed
and the upper internals
exposed,
personnel
quickly evacuated
the refueling cavity in keeping
with ALARA practices.
After plant personnel
removed the
head
from the cavity and
hoisted it over the operating
deck en route to the storage
stand,
the inspector
noted that
no one verified that the
IRVH was lifted a maximum of 12 inches
above the floor as
required
by precautions
in the procedure.
It appeared
to
the inspector located
across
the refueling cavity
approximately
50 feet away, that the head
was slightly more
than
12 inches off the ground.
During the Spring
1994
refueling outage,
contractor
personnel lifted the
head
more
than
2 feet off the ground to clear
a handrail
located
on
the refueling floor.
Last year's
action
was contrary to the
procedural
precaution
and resulted
in an Adverse Condition
Feedback
Report.
Because
the
head weighs approximately
180
tons,
the 12-inch limitation was
imposed for heavy load drop
considerations.
After the September
11 head-lift, the
inspector discussed
this year's
observation with licensee
management
who documented it in
a outage-improvement
CR.
Subsequent
IRVH manipulations
were performed with plant
personnel
verifying the
head to be
no more than
12 inches
off the ground while outside the cavity.
The inspector also noted
a few occurrences
of inappropriate
industrial safety acts
such
as individuals not tying off to
safety
ropes while standing
near the cavity.
These actions
were also noted
by the licensee's
NAS inspector at the job
site.
The
NAS inspector
was aggressive
in reminding workers
of safety requirements.
Despite the industrial safety
incidents
and the 12-inch verification issue,
the inspector
concluded that the overall
head lift was
done well.
WR/JO 95-ADIS1, Replace Battery
Bank 1A-SA
The inspectors
observed activities while the licensee
changed
out the sixty-cell safety-related
emergency
battery
1A.
The shop
had previously sent personnel
to the Robinson
plant to gain experience
by participating in a similar
13
activity there.
Based
on that experience,
the shop
had set
up
a small forklift in the battery
room to move the cells
between
the rack and
a conveyer extending
from the doorway
to
an area clear of the switchgear.
Battery cells
wer e
transferred
between
the conveyer
and turbine building
mezzanine
using
a small cart.
The licensee
had found, at
the Robinson plant, that carts with a simple swivel front
axle assembly
tended to turn over,
so they procure'd carts
with tierod-type steering for the Harris changeout.
Observed activities were being performed carefully and were
well controlled.
Subsequent
testing is discussed
in
paragraph
4.b.(4) of this report.
The applicable
vendor manual
stated that, if lubrication was
needed while sliding cells across
the plastic tray rail
covers,
use plain unscented
talcum powder.
This was to
preclude
long term chemical
reactions
between
powder
ingredients
and the polycarbonate
battery cell cases.
The
inspector
observed that, during removal of the old cells
from the old rail covers,
the licensee
was using
a barber
shop type powder with a number of ingredients - including
a
fragrance.
This had
been provided
by the system engineer.
After notification, the shop
ceased
using it during the
removal
process
and did not use
powder while installing the
new cells
on top of new rail covers,
thus reducing future
operability .uncertainty.
WR/JO 95-ABUG5, Containment
Equipment
Hatch Closure
Time
Test
The inspectors
observed
the licensee reinstall. the
containment
equipment
hatch
as
a "time test" to establish
a
baseline for future outages
when there
may be
a need to
conduct mid-loop operations
with the equipment
hatch
open.
The equipment
hatch
had not been
opened
since original
licensing
because
the personnel
hatch
was large
and
accommodated
most equipment.
During this outage,
the
equipment
hatch
was opened to pass
RCP deck plugs
and the
reactor cavity permanent
seal ring.
The hatch reinstallation
was controlled by procedure
CN-
N0100,
Rev. 3/2,
Containment
Equipment Hatch
Removal
and
Replacement,
sections
7.4 for immediate closure
and 7.3 for
normal closure'.
" Immediate closure" would result in the
hatch being closed
by 4 specific bolts (of 36).
The post-
trial assessment
was very good
and contained
many good
points for consideration,
As expected for a first-time
evolution, the test
showed that minor coordination
improvements
could
be readily made; that certain steps,
such
as platform removal, did not have
back
up provisions;
and
that using more than the TS-required
4 bolts might be
necessary
so that the remaining bolt holes would be
adequately
lined up in case additional bolts or full closure
were subsequently
necessary.
The licensee
did not have
a
need for the "immediate closure" provisions during this
outage.
The inspectors
had
no further comments
on this
test,
In general,
the performance of work was satisfactory with proper
documentation
of removed
components
and independent verification
of the reinstallation.
The inspectors identified no violations or
deviations in this area.
Surveillance
Observation
(61726)
The inspector
observed
several
surveillance tests to verify that
approved
procedures
were being used, qualified personnel
were
conducting the tests,
tests
were adequate
to verify equipment
operability, calibrated
equipment
was used,
and
TS requirements
were followed.
During the recent refueling outage,
the inspectors
observed
several
18-month
TS surveillance tests,
including the
following:
(1)
OST-1813,
Rev.
5,
Remote
Shutdown
System Operability.
This procedure partially satisfied
requirements
contained
in
TS 3/4.3.3.5,
Remote
Shutdown 'System.
The procedure
verified that transfer switches, Auxiliary Control
Panel
(ACP) controls,
and Auxiliary Transfer
Panel
controls were
operable for those
components
required
by the
SHNPP Safe
Shutdown Analysis to remove decay heat,
control
inventory through normal charging,
control
RCS pressure,
control reactivity,
and
remove decay heat via the
system.
The inspector
observed
portions of Test
C (section 7.3) of
this procedure,
which tested
the "B" train transfer panels,
and ATP-lBSB,
and associated
ACP control switches.
As directed
by the procedure,
operators
placed
each required
transfer
panel
switch in the
TRANSFER position
and later
verified that
ACP control switches
operated their respective
safe
shutdown
components.
Prior to the test performance,
as
an operator aid, plant personnel
placed
STAR placards
around
each control switch to be cycled,
ensuring that operators
cycled the right components
per the procedure.
While there
were
some unexpected
occurrences
during the procedure,
including blown-out indicating light bulbs
on the
ACP,
and
unanticipated
and actions regarding the
ESCWS
"
chiller condenser,
the few obstacles
were easily resolved
and the test
was successfully
completed.
The inspector
noted
good personnel
performance
during this surveillance
test.
15
OST-1823,
Rev. 8,
1A-SA Emergency
Diesel
Generator
Operability Test,
18 Honth Interval, Section 7.4.
This test procedure partially satisfied
18 month
surveillance
requirements
contained
in TS 4.8. 1. 1.2f.
Steps
in section 7.4 of the procedure verified that,
on
a
simulated loss of off-site power in conjunction with a
safety injection test signal,
the "A" emergency
bus
deenergized,
load shedding
occurred,
the "A" EDG started,
emergency
busses
were reenergized
in a timely manner,
and
emergency
loads
were energized
through the sequencer.
An
- essential
element of the test
was operators
simultaneously
simulating containment
spray actuation
and SI si.gnals,
while
manually tripping the normal electrical
feed from auxiliary
bus
D to emergency
bus A-SA.
During the initial performance of this test
on September
3,
operators
erroneously
performed the simulations first, then
opened
the normal circuit breaker.
This caused
the
sequencer
to start out on the incorrect
sequence
program,
then reset
and reinitiate using the correct program.
The
"A" RHR pump started
twice in about
a twenty second
interval.
The "A" containment
spray
pump failed to start
the
second
time.
The licensee
determined that the test
performance
did not satisfy the procedure
and that starting
the
RHR pump twice in twenty seconds
was contrary to
technical
requirements
in the manufacturer's
manual.
The
licensee
suspended
the test until September
4 ~
Having suspended
the test,
the l'icensee
evaluated
the
pump condition in
ESR 9500738,
Revisions
0 and
1
and
evaluated
the test control situation in
CR 95-2012.
These
evaluations
concluded that the
RHR pump
had not been
damaged
but that the test
should
be rerun.
The inspector
reviewed
the
and concluded that it reached
correct conclusions.
On September
4 morning, the inspector
observed
the test
being set
up again.
The prebriefing in the control
room was
well performed
and personnel
were dispatched
to stations.
The "B" RHR pump was already
stopped
and the
"A" pump was
stopped for the test,
allowing the reactor core to heat
up
at 30 'F per hour.
When the test participants did not
report to their stations
promptly, the
SCO aborted
the test,
restarted
A RHR pump to reestablish
core cooling,
and
initiated management
actions to improve personnel
performance.
The inspector
noted that the SCO's
response
was prompt
and appropriate,
Test section 7.4 was
successfully
completed later that day with all components
starting
as expected.
OST-1825,
Rev.
8, Safety Injection:
ESF Response
Time, Train
A 18 Nonth Interval
On
A Staggered
Basis,
Nodes 5-6.
16
This test procedure satisfied various
18 month
TS
surveillance
sections
requiring safety-related
equipment
response
to .test signals.
During the test,
the inspector
observed that components
actuated
as required.
The near
200-page
procedure
contained
some minor inadequacies,
and
there were
some personnel
errors
noted during its
performance.
Some of these resulted
in the procedure
having
to be temporarily revised
so that missed
elements of one
procedure
section
could be captured
in subsequent
sections.
In one case,
containment
fan cooler switches
were placed in
the wrong pretest position,
preventing the fans from
starting
on the SI signal
and requiring operators
to
reverify the fans would start in a later section.
In
another
case,
as discussed
in paragraph
4,c below,
a special
temporary procedure
(OST-9013T)
had to be developed
to
retest certain
AFW system valves.
The inspector,
however,
considered
the number of errors during OST-1825 performance
to be minimal considering
the procedure's
complexity.
Overall, licensee
performance
during this surveillance test
was adequate.
Additionally, plant equipment
responded
properly to the SI signals.
(4)
1E Battery Service Test,
[1A Battery]
1E Battery Performance
Test,
[1A Battery]
1E Battery 18-Month Test, [lA Battery]
CM-E0001, Station Battery Equalizing Charge,
[1A Battery]
These
procedures
were associated
with the installation
and
placing into service
the replacement
1A-SA battery.
The
inspectors
observed that procedures
were well run
and data
was properly collected.
During the first attempt to perform
shop personnel,
recognizing that the computerized
test
equipment
was not controlling the battery load
properly,
stopped
the test,
conferred with the test
apparatus
vendor,
and corrected
the setup.
The test
was
subsequently
performed without incident.
The inspectors
found satisfactory surveillance
procedure
performance with proper
use of calibrated test equipment,
necessary
communications
established,
notification/authorization
of control
room personnel,
and knowledgeable
personnel
having
performed the tasks.
The inspectors
observed
no violations or
deviations
in this area.
Effectiveness
of Licensee
Control in Identifying, Resolving,
and
Preventing
Problems
(40500)
Condition Report
CR 95-02534
was generated
after
an inadequate
surveillance test procedure
resulted
in
a partial safety injection
on October 5.
Temporary procedure
OST-9013T,
Temporary Procedure
for Testing the
MDAFW Pump
FCVs Auto Open Feature
From K635,
was
written to verify that the
AFW flow control valves would open
on
a
17
safety injection signal.
The valves'uto
open feature
was
originally supposed
to have
been tested earlier in the week during
the performance of safety injection test procedure
OST-1825.
However,
because
of an error in that procedure,
operators
did not
verify the valves
opened.
Specifically, the procedure
did not
take into account
the short duration (twenty seconds)
of the
valves'uto
open signal.
By the time OST-1825 directed operators
to verify the valves
opened,
the twenty second
signal
was gone
and
the valves
had reclosed.
Retest
procedure
OST-9013T
on October
5 directed
personnel
to
install jumpers
and lift leads,
ensuring all logic was satisfied
to open the valves
on
a safety injection signal.
Additionally,
the lifted leads
prevented
the signal
from actuating other safety
injection components,
such
as the emergency
safeguards
sequencer.
The procedure directed operators
to install
a switched jumper
between
two relay contacts
which,
upon closing the switch, would
initiate
a safety injection signal to the valve controllers.
Operators writing the procedure did not understand
that
a latching
r'clay in the circuit would necessitate
temporarily installing
another
jumper during test restoration
to remove the SI signal.
The procedure writers
assumed
that simply opening the switch on
the actuating
jumper would reset SI.
As directed
by the
procedure,
after the valves were satisfactorily tested
and with
the safety injection signal still present,
plant personnel
relanded
the previously lifted leads.
This action started
the
"B"
train Emergency
Safeguards
Sequencer
and sent start signals to
several
components
including the "B" RHR and
CCW pumps.
After
consulting with cognizant
engineers
and associated
drawings,
personnel
were able to remove the SI signal
and secure
the
affected
equipment.
The inspectors
noted that all equipment
started
as required following the partial SI.
Additionally, no
components
were
damaged
following the unexpected
actuation.
During subsequent
discussions
with licensee
personnel,
the
inspector determined
the root cause of this event to be inadequate
procedures
caused
by the operators
who wrote, reviewed,
and
approved
the procedure failing to fully understand
the equipment
function.
10 CFR 50, Appendix B, Criterion V, Instructions,
Procedures,
and
Drawings, requires,
in part, that activities affecting quality
shall
be prescribed
by documented
instructions,
procedures,
or
drawings, of a type appropriate
to the circumstances.
The
licensee's
Corporate guality Assurance
Program Hanual,
which
implements
the regulatory requirement,
states
in section 6.3.6
that provisions shall
be
made for the review of procedures
required
by plant commitment
by an individual knowledgeable
in the
area affected to determine
the
need for changes.
The failure to
have fully knowledgeable
procedure writers and reviewers for
procedure
OST-9013T is contrary to the
above requirements
and
resulted
in an unplanned
and partial safety injection.
18
This is identified as Violation 400/95-15-02,
Failure to Provide
for the Review of a Safety Injection Test Procedure
by an
Individual Fully Knowledgeable
in the System Logic.
The safety significance of this event
was minor.
The
RHR pump
operated
in recirculation
mode,
ensuring
minimum flow and
preventing
pump damage.
The charging/safety
injection
pump was
already operating for normal charging
when the SI occurred.
Operators verified that all equipment started
as required
on the
SI signal,
and were later able to reset SI.
At the close of the
inspection period,
the licensee
was still developing corrective
actions.
This event
was properly reported to the
NRC in accordance
with
10 CFR 50,72 requirements.
A 30 day
LER was pending at the end of
the inspection
periods
Overall,
one violation was identified in the maintenance
and
surveillance
area.
Otherwise,
surveillance
and maintenance
procedures
were performed effectively with only minor issues
requiring resolution.
ENGINEERING
a o
Design
and Installation of Plant Modifications (37551)
ESRs involving the installation of new or modified systems
were
reviewed to verify that the changes
were reviewed
and approved
in
accordance
with 10 CFR 50.59, that the changes
were performed
in
accordance
with technically adequate
and approved
procedures,
that
subsequent
testing
and test results
met approved
acceptance
criteria or deviations
were resolved
in an acceptable
manner,
and
that appropriate
drawings
and facility procedures
were revised
as
necessary.
The licensee
was challenged with many issues
requiring
engineering resolution during the outage.
The following
engineering
evaluations,
modifications,
and/or testing in progress
were inspected.
(1)
ESR 9400013,
Permanent
Cavity Seal
Ring
This design
package
provided engineering
instructions for
installing the
new permanent refueling cavity seal ring.
For previous refueling outages,
the licensee
installed
a
temporary
seal
ring with inflatable bladders
which consumed
a lot of outage
time and personnel
dose.
The
new seal, ring,
which would be permanently
welded to the cavity and reactor
vessel,
would eliminate recurring installation
and removal
hassles.
The
new design would include several
removable
hatch covers allowing proper ventilation for RCS components
located in the reactor cavity annulus
area.
19
Due to fitup problems,
the
new seal ring project was
abandoned
and the licensee
resorted
to using the old
inflatable seal ring for cavity floodup prior to core reload
during this outage.
Specific problems
centered
around the
seal
ring not fitting properly between
the reactor vessel
seal
ledge
and the cavity liner.
Additionally, there were
problems
achieving proper clearances
between
the three major.
sections of the ring.
Proper clearances
were necessary
for
welding the three sections
together
and welding the ring to
the cavity liner and vessel
ledge.
Following the unexpected
installation delays
and eventual
project abandonment,
the
licensee initiated
a Condition Report
and
a root cause
investigation into contributing factors.
The inspectors
observed
part of the attempted installation,
reviewed portions of the design
package,
and concluded that
neither poor workmanship nor poor engineering
contributed to
the project failure.
The design
package
was adequately
detailed with specific installation instructions,
adequate
drawings,
and
a good unreviewed safety question
determination.
With a piece of equipment
as large
and
complex
as the
new cavity seal ring, which was manufactured
offsite by
a vendor, fitup problems like these
were
possible.
Licensee
management
informed the inspector that
the permanent
seal
ring installation would be attempted
again during the next refueling outage.
ESR 9500876,
Stuck Reactor
Vessel
Closure
Stud
0'40
This
ESR documented
the acceptability of a reactor vessel
head
stud
840 which became
stuck during reinstallation
on
October
2.
When the stud
became
stuck,
personnel
could not
obtain full stud
engagement
into the reactor vessel,
Actual
stud
engagement
was approximately 6.625 inches vice the
standard
of 7,375
inches for 5-13/16 inch diameter studs.
The engineering
evaluation
considered
the engagement
deviation
and the fact that the stuck stud could not be
removed for required
ASHE Section
XI inspection.
From
calculations,
engineers
determined that the stud could still
be normally tensioned
along with the remaining studs,
and
the stresses,
either
from the tensioning or the pending
heatup,
would not exceed effective code allowables.
Additionally, since the 10-year inspection
would not be due
until 1997,
the stud could remain in the vessel
during the upcoming operating cycle.
The inspector
considered
the evaluation to be adequate.
ESR 9500738,
Rev.
0 and
Rev.
1,
RHR Pump
A Starting
Frequency
This
ESR evaluated
the effect of having the "A" RHR pump
start twice in twenty seconds
during the OST-1823
4
20
performance
discussed
in paragraph
4.b.(2) of this report.
The main concern
was whether or not the
pump starts
imposed
excessive
heat stresses
on the motor.
The evaluation
roughly equated
the rate of heat production during the first
stages
of motor acceleration
to that generated
in
a stall
condition.
Engineers
then obtained
the
maximum safe stall
time (ten seconds)
for the
RHR pump motor from the
associated
plant specification.
Plant engineers
assumed
that heat stresses
on the motor in a stall event would
envelope
the heating
experienced
in an acceleration
event of
equal duration.
With the acceleration
time for the
pump
motor being 0.8 seco'nds,
two start events
would equal
1.6
seconds
which was within the ten second
maximum safe stall
time.
Thus, the evaluation
concluded that the motor was not
overstressed
by the two starts.
Revision
0 of the
contained
an error regarding
the time between
the two
starts.
Plant personnel
detected
the error
and corrected it
in Rev.
1.
The inspector considered
this evaluation to be
adequate.
ESR 9500752,
CSIP
1B-SB Safety Significance of Stuck
Miniflow Check Valve
As discussed
in paragraph
3.a,(1) of this report,
the "B"
CSIP miniflow check valve
1CS-193 failed
a forward flow test
due to
a stuck disk inside the valve.
One of the valve's
safety functions
was to pass
at least
60
gpm forward flow
during
a safety injection to prevent
pump damage.
The "B"
pump was erroneously
placed in service for seven
hours
during
Mode
4 on September
2 with the valve in the degraded
condition.
'The
ESR analyzed
the condition for a postulated
LOCA and inadvertent
SI.
These
were the most limiting
events possibly requiring the miniflow system to function
with the plant in Mode
4 and
RCS pressure
reduced to
approximately
350 psig.
After considering
the. plant
operating conditions at the time and the availability of
other systems,
the evaluation
concluded that the
pump would
have performed its intended safety injection function and
would not have
been
damaged without the miniflow system
available.
The evaluation further showed that the
pump
never operated
in Mode
4 on September
2 pumping less
than
the
60 gpm minimum recommended
by the pump's vendor,
The
inspector
considered this evaluation to be adequate.
As
mentioned
in report paragraph 3.a.(l), the licensee
reported
the check valve deficiency in accordance
with 10 CFR 21.21.
ESR 9500098,
Rev.
0, Closed Cell 'Tubing/Sheet
Type
Insulation Evaluation.
This
ESR evaluated
the use of closed cell tubing
and sheets
for anti-sweat insulation for essential
and nonessential
.
chilled water piping greater
than five inches in diameter.
21
This had
been previously approved
by licensee
engineers
in
PCR 7346 (October
1994) for pipe less
than five inches
diameter.
This subject
had attracted
the inspectors
attention
when they happened
upon
a "Transient Combustible"
tag hanging
on
a permanent
insulation installation in August
1995.
The
ESR specifically evaluated
two aspects
of the
insulatidn.
First was thermal conductivity, which was about
twice as high
as the currently used fiberglass insulation.
Heat gain from the
room would be offset by
a lower load
on
the
HVAC units cooling the room.
The inspector
concluded
that this was
a reasonable
approach that demonstrated
understanding
of the systems
and building environment.
Second
was the change
in fire loading caused
by changing
from fiberglass material to hydrocarbon
(plastic) material.
The
ESR concluded that the material
was not combustible
based
on statements
in
NRC
CMEB 9.5-1.
This meant that
room fire loading would not require updating
when the
material
was installed.
In contrast to this evaluation,
the
licensee's
applicable
Chemical
and Consumables
Fact Sheet,
AP-501-01059
Revision
1, stated that the material
was'ombustible.
That was the reason for the "Transient
Combustible" tag hanging
on
a permanent
insulation
installation.
The inspector
reviewed the relevant
literature
and concluded that the
ESR conclusion
was flawed.
The
BTP defines
a number of noncombustible
materials
and
then states
that they
may have
a thin coating,
not over I/8
inch thick, of material with fire properties similar to
this.
This material
is about
one .inch thick, not fitting
the
BTP exception.
Thus, this material
was clearly
flammable.
When informed of the
NRC conclusion,
the
licensee
proceeded
to recalculate
the fire loading of
affected locations.
ESR 9500809,
As-found Set Pressure
of Valve 1RC-127 out of
Tolerance
This evaluation
evaluated
the acceptability of valve test
results
from September
13 which were outside of set pressure
acceptance
criteria.
Specifically, pressurizer
code safety
valve
1RC-127 is required
by TS 3.4.2.2 to be operable
having
a lift setpoint of 2485 psig with a margin of plus or
minus
one percent.
The upper margin limit equates
to
2509.85 psig.
The valve was shipped to
a contract
laboratory
and later failed its initial test
by lifting at
2516 psig.
Three
subsequent
tests
revealed lift pressures
of 2493,
2487,
and
2482 psig.
The licensee's
evaluation
stated that the initial failure
was probably caused
by shipping problems.
This was
supported
by the three consecutive
acceptable
tests.
22
b.
Nevertheless,
the evaluation appropriately
considered
the
effects of the valve lifting at 2516 psig during the most
limiting overpressurization
design basis
accident
(a main
The evaluation
showed that if the valve
lifted at 2516 psig,
RCS pressure
would still be maintained
less
than
110 percent of design
(2750 psig) with margin
remaining.
The evaluation took credit for proper operation
of the other two safety valves.
The inspectors
considered
this evaluation to be adequate.
The inspectors
identified no violations or deviations
in the
design/installation/testing
of modifications area.
Review of LERs (92700)
(Open)
LER 95-006-00,
Emergency
Core Cooling System Piping Not
Fully Contained Within Reactor Auxiliary Building Emergency
Exhaust
System
Boundary,
Resulting in Condition Outside
Design
Basis.
This
LER discussed
the Reactor Auxiliary Building Emergency
Exhaust
System construction deficiency which resulted
in certain
portions of the
ECCS being outside of the emergency ventilation
boundary.
This issue is discussed
in more detail in NRC IR
400/95-13.
The
LER will remain
open pending licensee
completion
and inspector review of the root cause
investigation
and
associated
corrective actions.
The licensee
intended to
supplement
the
LER when the root cause
investigation
was
completed.
Overall, engineering activities were performed well, especially
considering
the
many engineering
challenges
that were presented
during
the refueling outage.
The inspectors
identified no violations or
deviations
in the engineering
area.
PLANT SUPPORT
b.
Plant Housekeeping
Conditions
(71707) - The inspectors
reviewed
storage of material
and components,
and observed
cleanliness
conditions of various
areas
throughout the facility to determine
whether safety hazards
existed.
With the plant in a refueling
outage,
much of the plant was staged
at various times with
scaffolding for maintenance activities.
At various times,
unused
was stored throughout the plant in designated
storage
locations.
Plant equipment that was not part of some work scope
was in generally
good condition.
Overall, plant equipment
and
overall
housekeeping
was adequate
during the outage.
The
inspectors
observed
no safety hazards.
Radiological
Protection
Program
(71750) - The inspectors
reviewed
radiation protection control activities to verify that these
activities were in conformance with facility policies
and
23
procedures,
and in compliance with regulatory requirements.
The
inspectors
also verified that selected
doors which controlled
access
to very high radiation areas
were appropriately locked.
Radiological
postings
were likewise spot checked for adequacy.
Since this was
an outage
month, the inspectors particularly
focused
on licensee
controls for containment entries
and hot work.
A containment
entry window was
manned
around the clock by
personnel
keeping track of workers inside containment.
For major
jobs like the
IRVH lift and other core manipulations,
HP personnel
were present,
ensuring worker exposure
was minimized.
The
licensee
spent less worker dose during the initial vessel
head
lift than in any year before.
Operators
made
good
use of remote
dosimetry monitoring technology for the steam generator jobs.
To
better control worker exposure,
the licensee
established
communications
between
workers in high exposure
areas
and
personnel
in remote locations.
The licensee
bettered its dose
. goal
by over
16 person-rem,
reaching
142.7 person-rem
vs.
a goal
of 159.3 person-rem.
Unfortunately,
the number of personnel
contamination
events
(PCEs) during the outage
exceeded
the
licensee's
outage
goal
by 22
(122 vs.
100).
Although the licensee
investigated
each
as it occurred,
the licensee's
investigation
into the excessive
total
was continuing at the
end of the
inspection.
Each
PCE was appropriately
documented
on
a condition
report.
Overall, the inspector considered
outage
performance
in
radiological controls to be good.
Security Control
(71750) - During this period,
the inspectors
toured the protected
area
and noted that the perimeter
fence
was
intact
and not compromised
by erosion or disrepair.
The fence
fabric was secured
and barbed wire was angled.
Isolation zones
were maintained
on both sides of the barrier
and were free of
objects
which could shield or conceal
an individual.
The
inspectors
observed
various security force shifts perform daily
activities,
including searching
personnel
and packages
entering
the protected
area
by special
purpose detectors
or by
a physical
patdown for firearms,
explosives,
and contraband.
Other
activities included vehicles
being searched,
escorted,
and
secured;
escorting of visitors; patrols;
and compensatory
posts.
In conclusion,
the inspectors
found that selected
functions
and
equipment of the security program complied with requirements.
Fire Protection
(71750)
The inspectors
observed fire protection
activities, staffing
and equipment to verify that fire alarms,
extinguishing equipment,
actuating controls, fire fighting
equipment,
emergency
equipment,
and fire barriers
were operable.
During plant tours,
the inspector
looked for fire hazards.
The
inspector
concluded that the fire equipment
and barriers
inspected
were in proper physical condition.
As stated
in paragraph
3.e of
24
this report, plant response
to
a perceived
switchgear fire was
excellent.
e.
Emergency
Preparedness
(71750)
The inspectors
toured
emergency
response facilities to verify availability for emergency
operation.
Duty rosters
were reviewed to verify appropriate
staffing levels were m'aintained.
As applicable,
the inspectors
observed
emergency
preparedness
exercises
and drills to verify
response
personnel
were adequately trained.
No emergency
preparedness
exercises
or drills were performed during this
inspection period.
Plant Nuclear Safety
Committee Meetings
(40500) - The inspectors
attended
several
PNSC meetings during the refueling outage to
verify effectiveness
of the licensee's
onsite safety committee.
These
meetings
discussed
a wide range of plant issues
including
some discussed
earlier in this report:
midloop operations,
containment
hatch closure,
and
a reactor vessel
stuck stud.
The
inspector
noted that
a
PNSC quorum was always present
and that
qualified individuals were
on the committee.
The inspector
reviewed selected
meeting minutes
and determined that they were
adequate.
The inspector
noted that committee
members
had the
necessary
safety focus during the meetings.
The inspectors
found plant housekeeping
and material condition of
components
to be satisfactory.
The licensee's
adherence
to radiological
controls,
security controls, fire protection requirements,
emergency
preparedness
requirements,
and
TS requirements
in these
areas
was
satisfactory.
The inspectors
identified no violations or deviations
in
the plant support
area.
EXIT INTERVIEW
The inspector
met with licensee
representatives
(denoted
in paragraph
1)
at the conclusion of the inspection
on October 6,
1995.
'During this
meeting,
the inspectors
summarized
the scope
and findings of the
inspection
as they are detailed in this report, with particular emphasis
on the Violations and
LERs addressed
below.
The licensee
representatives
acknowledged
the inspector's
comments
and did not
identify as proprietary
any of the materials
provided to or reviewed
by
the inspectors
during this inspection.
No dissenting
comments
from the
licensee
were received.
Item Number
Status
Descri tion and Reference
95-015-01
95-015-02
Open
Open
Failure to Properly Annotate
Surveillance Test Requirement
for an Inoperable
CSIP,
paragraph 3.a.(l).
Failure to Provide for the
Review of a Safety Injection
95-011-01
95-006-00
95-007-00
95-008-00
Closed
Open
Open
Closed
25
Test Procedure
by an
Individual Fully Knowledgeable
in the System Logic, paragraph
4.c.
IFI
guestionable
Position
Indication for Containment
Isolation Valve 1SP-209,
paragraph
3.g.
LER
Emergency
Core Cooling System
Piping Not Fully Contained
Within Reactor Auxiliary
Building Emergency
Exhaust
System
Boundary,
Result'ing in
Condition Outside
Design
Basis,'aragraph
5.b.
LER
Inadvertent Start of the
Turbine Driven AFW
Pump/Unplanned
ESF Actuation
and Identification of an,
Additional Related Test
Deficiency, paragraph 3.f.(l).
LER
"B" Charging/Safety
Injection
Pump
wa's Returned to Service
Prior to Required
Acceptance
Testing,
Resulting in
Technical Specification
Violation, paragraph 3.f.(2).
ACRONYMS AND INITIALISMS
ALARA-
CFR
CR
CSIP
EIR
encl
ESCWS
'SF
Auxiliary Control
Panel
As
Low as Reasonably
Achievable
American Society of Mechanical
Engineers
Branch Technical
Position
Component
Cooling Water
Code of Federal
Regulations
Corrective Maintenance
[procedure]
Carolina
Power
& Light
Condition Report
Charging/Safety
Injection
Pump
Chemical
and
Volume Control
System
Emergency
Core Cooling System(s)
Emergency Diesel
Generator
Equipment
Record
Enclosure
Essential
Services
Chilled Water System
Engineered
Safeguards
Feature
26
0 F
FR
GPM
IFI
IR
IRVH
IS I
LCO
LER
NAS
NPF
NRC
OMM
OST
PIG
PNSC
pslg
RII
SCO
TADOT
TS
vs
WR/JO
Engineering
Service
Request
Emergency Service
Water
Degrees
Fahrenheit
Flow Control Valve
Fuel Handling Procedure
Federal
Register
General
Procedure
Gallons
Per Minute
Heating, Ventilation,
and Air Conditioning
Inspector
Followup Item
[NRC] Inspection
Report
Integrated
Reactor
Vessel
Head
Inservice
Inspection
Limiting Condition for Operation
Licensee
Event Report
Loss of Coolant Accident
Low-Temperature
Overpressure
Protection
Motor-Driven Auxiliary Feedwater
[pump]
Maintenance
Surveillance Test [procedure]
Nuclear Assessment
Section
Nuclear Production Facility [a type of license]
Nuclear Regulatory
Commission
Nuclear Reactor Regulation
NRC Technical
Report Designation
Operations
Management
Manual
Operations
Surveillance
Test [procedure]
-Personnel
Contamination
Event
Plant
Change
Record
Public Document
Room
Particulate,
and
Gas [monitor]
Plant Nuclear Safety Committee
Power-Operated
Relief Valve
Pounds
per Square
Inch,
Pump
Residual
Heat
Removal
Region
Two
[NRC Office]
Senior Control Operator
Safety Injection
Trip Actuating Device Operational
Test
Turbine-Driven Auxiliary Feedwater
[pump]
Technical Specification [part of the facility license)
Violation [of NRC requirements]
Versus
Work Request/Job
Order