ML18011A529

From kanterella
Jump to navigation Jump to search
Insp Rept 50-400/94-13 on 940604-0701.No Violations Noted. Major Areas Inspected:Plant Operations,Review of Nonconformance Repts,Maint Observation,Surveillance Observation,Design & Testing of Mods & Fire Protection
ML18011A529
Person / Time
Site: Harris 
Issue date: 07/25/1994
From: Tedrow J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML18011A527 List:
References
50-400-94-13, NUDOCS 9408090157
Download: ML18011A529 (24)


See also: IR 05000400/1994013

Text

~S AECy

~4

0

Cy

0O

UNITED STATES

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTASTREET, N.W., SUITE 2100

ATLANTA,GEORGIA 303234199

Report No.:

50-400/94-13

Licensee:

Carolina

Power

and Light Company

P. 0.

Box 1551

Raleigh,

NC 27602

Docket No.:

50-400

Facility Name:

Harris

1

Inspection

Conducted:

June

4 - July 1,

1994

Inspectors:

J.

e

w, Senio

Re ident Inspector

License No.:

NPF-63

Da e Signed

D.

R

rts

Resident

Inspector

Approved by:

H. Christensen,

Acting Chief

Reactor Projects

Branch

1

Division of Reactor Projects

D te

S gned

'!~l>~

Date Signed

SUMMARY

Scope:

This routine inspection

was conducted

by two resident

inspectors

in the areas

of plant operations,

review of nonconformance

reports,

maintenance

observation,

surveillance observation,

design

and testing of modifications,

plant housekeeping,

radiological controls, security, fire protection,

emergency

preparedness,

review of licensee

event reports,

and licensee

action

on previous inspection

items.

Numerous facility tours were conducted

and

facility operations

observed.

Some of these tours

and observations

were

conducted

on backshifts.

Results:

Two violations were identified:

Failure to preplan

non-emergency

work,

paragraph 3.a(2);

Failure to calibrate

a high voltage probe measuring

device,

paragraph 3.b(l).

A non-cited violation regarding the failure to maintain configuration control

of a valve in the high head safety injection system,

paragraph

2.b.

9408090i 57 940725

PDR

ADOCK 05000400

PDR

2

Deficiencies

were noted in scheduling safety-related

work/testing,

paragraph

3.a(1),

and during the observation of a practice

emergency drill, paragraph

5.e.

The design of the spent fuel pools

and cooling systems

was adequate

and

operation

was satisfactory,

paragraph

5.b(1).

The licensee's

efforts to

minimize radiation exposure

during the annual

spent fuel shipping cask

inspections

were successful,

paragraph

5.b(2).

REPORT DETAILS

1.

Persons

Contacted

2.

Licensee

Employees

  • D. Batton,

Manager,

Work Control

D, Braund,

Manager,

Security

  • B. Christiansen,

Manager,

Maintenance

  • J. Collins, Manager, Training

J.

Dobbs,

Manager,

Outages

  • J. Donahue,

General

Manager,

Harris Plant

H.

Hamby,

Manager,

Regulatory Compliance

  • D. HcCarthy,

Manager,

Regulatory Affairs

  • J. Nevill, Manager,

Technical

Support

  • R. Prunty,

Manager,

Licensing

5 Regulatory

Programs

  • W. Robinson,

Vice President,

Harris Plant

  • W. Seyler,

Manager,

Project

Management

  • D. Tibbitts, Manager,

Operations

B. White, Manager,

Environmental

and Radiation Control

  • 0. Wilkins, Manager,

Spent

Fuel

M. Worth, Manager,

Onsite Engineering

Other licensee

employees

contacted

included office, operations,

engineering,

maintenance,

chemistry/radiation

and corporate

personnel.

  • Attended exit interview

Acronyms

and initialisms used throughout this report are listed in the

last paragraph.

Operations

'a

~

Plant Operations

(71707)

The plant continued in power operation

(Hode 1) for the duration

of this inspection period.

(1)

Shift Logs and Facility Records

r

The inspector

reviewed records

and discussed

various entries

with operations

personnel

to verify compliance with the

Technical Specifications

(TS)

and the licensee's

administrative procedures.

The following records

were

reviewed:

shift supervisor's

log; control operator's

log;

night order book; equipment

inoperable record; active

clearance

log; grounding device log; temporary modification

log; chemistry daily reports; shift turnover checklist;

and

selected

radwaste

logs.

In addition, the inspector

independently verified clearance

order tagouts.

The inspectors

found the logs to be readable,

well

organized,

and provided sufficient information on plant

status

and events.

Clearance

tagouts

were found to be

properly implemented.

No violations or deviations

were identified.

Facility Tours

and Observations

Throughout the inspection period, facility tours were

conducted

to observe activities in progress.

Some of these

observations

were conducted

during backshifts.

Also, during

this inspection period, licensee

meetings

were attended

by

the inspectors

to observe

planning

and management

activities.

The facility tours

and observations

encompassed

the following areas:

security perimeter fence; control

room;

emergency

diesel

generator building; reactor auxiliary

building; waste processing

building; turbine building; fuel

handling building; emergency

service water building; battery

rooms; electrical

switchgear

rooms;

and the technical

support center.

During these tours,

observations

were

made regarding

monitoring instrumentation

which included equipment

operating status,

electrical

system lineup, reactor

operating

parameters,

and auxiliary equipment operating

parameters.

Indicated parameters

were verified to be in

accordance

with the

TS for the current operational

mode.

The inspectors

also verified that operating shift staffing

was in accordance

with TS requirements

and that control

room

operations

were being conducted

in an orderly and

professional

manner.

In addition,

the inspector

observed

shift turnovers

on various occasions

to verify the

continuity of plant status,

operational

problems,

and other

pertinent plant information during these turnovers.

The

licensee's

performance

in these

areas

was satisfactory.

Since the plant startup

from the refueling outage,

the

inspectors

have noted

increased

seal

leakage

from the "A"

and "B" Charging/Safety

Injection Pumps.

During this

inspection period, licensee

personnel

attempted

to reduce

the seal

leakage

from the "A" CSIP but were only partially

successful.

The "B" CSIP will be worked following

completion of repairs to "A" CSIP.

The excessive

seal

leakage

does not adversely effect

pump operation.

No violations or deviations

were identified.

Review of Nonconformance

Reports

(71707)

Adverse Condition Feedback

Reports

were reviewed to verify the

following:

TS were complied with, corrective actions

and generic

items were identified and items were reported

as required

by

10 CFR 50.73.

ACFR 94-2263 discussed

an incident involving poor configuration

control which was discovered

by an Auxiliary Operator.

During

performance of rounds

on June

21, the

AO heard flow noise through

the normal miniflow line for the "8" CSIP which was not operating.

The

AO found valve 1CS-750,

"C" CSIP Alternate Hiniflow Hanual

Isolation to "8" Header,

unlocked

and turned about

a quarter turn

off of its seat.

Further investigation

by the operator determined

that the valve was required to be locked closed for the existing

operating condition ("C" CSIP in service replacing the "A" pump)

by procedure

OP-107,

Chemical

and Volume Control

System.

The

valve served to maintain train separation

between

the "8" and

"C"

pumps'lternate

miniflow lines when both

pumps were aligned to

start

on

a safety injection signal.

On June

22,

an operator

was

dispatched

to shut

and lock the valve.

The operator

was

successful

in closing the valve,

but flow noise

was still detected

in the line indicating that there

was leakage

past the valve seat.

Following identification of the valve position discrepancy,

several

actions

were taken.

Licensee

personnel

reviewed control

room logs, valve line-ups,

and equipment clearance

records for the

previous

two months to determine

the cause of the valve being in

the incorrect position.

The valve lineup sheets

indicated that

the valve was last checked to be locked shut

on Hay 3,

1994.

The

inspectors

interviewed licensee

personnel

who indicated that valve

1CS-750

was also observed

to be locked shut just days before the

June

21 incident when operators

were at the valve hanging

a

deficiency tag addressing

valve stem leakage.

At the close of the

inspection period, licensee

personnel

had not determined

why the

valve was not in the configuration required

by the operating

procedure.

Licensee

personnel

conducted

an operability determination

in

accordance

with procedure

THH-408, Operability Determination,

which concluded that the degraded

component

could still perform

its intended safety function without any compensatory

actions.

Specifically, it was concluded that since the miniflow lines are

isolated during Safety Injection, seat

leakage

by valve 1CS-750

was not

an immediate safety concern.

Valve leakage

would be

unexpected

during dual

pump operation with the "8" and

"C"

alternate miniflow paths fully pressurized

by their respective

pumps.

For the postulated

scenario of an inadvertent

SI

and main

steamline

break,

any additional valve leakage

under single

pump

operation

would not be detrimental.

Therefore,

the safety

significance of this incident was minor.

Operating

procedure

OP-107 requires

1CS-750 to be locked closed

when the

"C" CSIP is in service replacing the "A" CSIP.

The

position of valve

1CS-750 identified by licensee

personnel

on June

21 is contrary to that requirement

and is considered

to be

a

violation.

This violation will not be subject to enforcement

action because

the licensee's

efforts in identifying and

correcting the violation meet the criteria specified in Section

VII.B of the Enforcement Policy.

Non-cited Violation (400/94-13-01):

Failure to maintain

configuration control for alternate miniflow valve 1CS-750.

Corrective actions for the above incident included issuance

of an

Operations

Night Order,

on July 8, discussing

the event

and

reinforcing the need to check procedures

for configuration

control.

Licensee Action on Previously Identified Operations

Inspection

Findings

(92901)

(Closed) Violation 400/94-05-01:

Failure to implement procedures

adequately.

The inspector

reviewed

and verified completion of the corrective

actions listed in the licensee's

response letter dated April 8,

1994.

The following actions

were accomplished:

~

For the filter backflush evolution, night orders

were

written to emphasize

clear communications

among operating

personnel

during filter backflush evolutions.

Individuals

were counseled,

and operating

procedures

were revised to

specify single point accountability

and control of the

activity.

For the cold weather event,

licensee

personnel

performed

an

engineering

evaluation

which concluded that equipment in the

ESW structures

could operate

properly with air temperatures

as low as

32 degrees

F.

Procedure

AP-301, Adverse Weather

Operation,

was revised to reference

a list of heaters

and

the method to be used to verify proper operation.

Annual

inspections of the heaters

have

been established

and

scheduled for performance prior to cold weather.

Increased

emphasis will be provided

on deficiencies identified by

these corrective actions.

For the wiring identification problem, training was provided

to craft personnel

and to quality control inspectors

on the

requirements

of procedure

EM-003, Termination

and Testing

Wire and Cable.

This training included contractors utilized

for the last refueling outage

and

a provision was

implemented to ensure this training is provided

on

a

recurrent basis.

3.

Maintenance

'a ~

Maintenance

Observation

(62703)

The inspector observed/reviewed

maintenance activities to verify

that correct equipment

clearances

were in effect; work requests

and fire prevention work permits were issued

and

TS requirements

were being followed.

Maintenance

was observed

and work packages

were reviewed for the following maintenance activities:

Repair mechanical

seal

leak on the "A" CSIP, in accordance

with procedure

CH-H0019, Pacific Charging/Safety

Injection

Pump Size 2-1/2"

RL Type IJ Disassembly

and Maintenance.

Preventive

maintenance

on safety

bus lA-SA overcurrent

relays in accordance

with procedure

MPT-E0022,

General

Electric Overcurrent

IFC-53 (Safe

Shutdown)

Relay

Calibration.

Inspect

sump lube oil cooler for the "8" CSIP.

~

Troubleshoot

RCS Flow Loop 3,

Channel II to determine

why

channel failed low, using procedure

HST-I0062,

Reactor

Coolant

Flow Instrument

(F-0435) Calibration.

~

Replace

selector

valve for leaking lube oil duplex filter on

the "B" Emergency

Diesel

Generator

(EDG) in accordance

with

procedure

HPT-M0028,

Emergency Diesel

Generator

Lube Oil

Full Flow Filter Inspection

and Cleaning.

~

Remove the turbine driven auxiliary feedwater

pump suction

relief valve

1CE-1159

and verify setpoint in accordance

with

procedure

EST-211, Auxiliary Relief Valve Testing.

In general,

the performance of work was satisfactory with proper

documentation of removed

components

and independent verification

of the reinstallation.

(1)

Two ACFRs were generated

concerning the poor scheduling of

emergent

work.

Both ACFRs 94-2224

and 94-2231 discussed

situations

where emergent

work was scheduled

simultaneously

with previously scheduled

work affecting opposite train

components.

Specifically,

ACFR 94-2224 documented that

on

June

13, work was

added to the schedule

which required the

removal of safety-related

air handler

AH-15B from service

while the "A" EDG was

removed from service.

Since this

action would have resulted

in a support

system for the other

train

EDG being unavailable,

both

EDGs would have

been

considered

inoperable.

ACFR 94-2231

documented

that three

days later, while air handler

AH-15B was inoperable,

a

prescheduled

TS surveillance test affecting the "A" train

solid state protection

system could not be performed.

While not documented

in an

ACFR, the inspector

was informed

of another

example of poor scheduling

on June

23.

While

various

"B" train systems,

including Emergency Service

Water,

were out-of-service for a preplanned train outage,

work on valve

1SW-20,

which is an "A" train

ESW pump

discharge strainer backflush valve,

was scheduled

and

discussed

in the manager's

morning meeting minutes

as

an

immediate attention

item.

The mechanic working this job

called the control

room and

asked if the valve could be

stroked closed,

rendering the "A" ESW system inoperable.

Permission

was denied thereby avoiding

a TS 3.0.3 entry.

The operators

were diligent in preventing conflicting train

work activities for the two cases

documented

in the above

ACFRs.

The inspectors

have

documented

other

examples of

poor scheduling

in

NRC Inspection

Reports

50-400/94-05

and

50-400/93-21.

Those reports

discussed

the poor scheduling

of maintenance

on heating

and ventilation systems

and

unnecessary

out-of-service times.

During

a review of the shift supervisors

log, the inspector

noted that

on June

29,

1994, priority "E" work had

been

authorized to open the "A" ESW strainer backflush valve

1SW-

20 which had failed closed.

Priority "E" emergency

work

could be authorized to begin prior to planning being

completed

and documented after the fact.

Maintenance

was in

progress

on

a "B" train control

room emergency ventilation

system

component.

Since the service water valve affected

"A" ESW cooled components,

the associated chiller for the

"A" control

room emergency ventilation system

was considered

to be unavailable.

Plant operators

therefore

entered

TS 3.0.3

due to both control

room emergency ventilation systems

being inoperable.

Technical specification 3.0.3 requires

that the plant

be shutdown to hot standby within seven

hours

followed by cold shutdown within 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />.

The emergency

work was authorized to avoid the unnecessary

plant transient

which would result from fulfillingthe

TS 3.0.3 action

statement.

Procedure

PLP-710,

Work Management

Process,

Attachment

5, allowed the shift supervisor to initiate

emergency

work whenever

TS 3.0.3

was entered.

The inspector discussed

this activity with licensee

personnel.

The actual

work performed

on this safety-related

valve involved the removal of instrument air tubing from the

top of the valve actuator, reinstalling

a failed air line,

and removing instrument tubing from the associated

solenoid

valve and regulator.

This work succeeded

in opening the

valve and overrode the valve actuator

such that the valve

remained

opened.

During the event review for reportability determination,

licensee

personnel

determined that

TS 3.0.3

was not

applicable for this situation,

and therefore the event

was

not reportable.

The inspector

concluded that the failure of

valve

1SW-20 was actually not

an emergency situation

and

therefore appropriate

preplanning

should

have

been

accomplished.

Failure to properly implement the

requirements

of procedure

PLP-710 to preplan

non-emergency

work is contrary to the requirements

of TS 6.8. l.a and is

considered

to be

a violation.

Violation (400/94-13-02):

Failure to preplan

non-emergency

work on valve

1SW-20.

Surveillance Observation

(61726)

Surveillance tests

were observed to verify that approved

procedures

were being used; qualified personnel

were conducting

the tests;

tests

were adequate

to verify equipment operability;

calibrated

equipment

was utilized;

and

TS requirements

were

followed.

The following tests

were observed

and/or data reviewed:

~

MST-I0140

Delta T/Tavg Loop (T-0412) Operational

Test

~

HST-I0208

Pressurizer

Level

Loop (L-0459) Operational

Test

~

MST-I0071

Neutron Flux Monitoring System Train A (NI-60)

Source

Range Calibration

~

MST-I0125

Hain Steamline

Pressure,

Loop

1 (P-0474),

Operational

Test

~

OST-1026

Reactor Coolant System

Leakage

Evaluation Daily

Interval

The performance of these

procedures

was generally found to be

satisfactory with proper

use of calibrated test equipment,

necessary

communications

established,

notification/authorization

of control

room personnel,

and knowledgeable

personnel

having

performed the tasks.

(1)

During the performance of procedure

HST-I0071

on June

17,

1994, the inspector

observed

the technicians

measure

the

detector

high voltage

power supply.

Section

7. 1.3 of the

procedure directed the technicians

to connect

a high voltage

probe to the center conductor of the triax connector

and

a

digital voltmeter to the connector outer shield.

The

acceptance

criteria for these

steps listed

784 - 816

VDC for

the high voltage

and 300 - 340

VDC for the loss of high

voltage alarm setpoint.

Actual voltage measured

on the

digital voltmeter was 0,800

VDC and 0.322

VDC respectively

(0 - 20

VDC scale).

The inspector

asked the technicians

about the measured

voltages

and

was informed that the high

voltage probe included

a division ratio of 1000: 1 and that

the voltage readout displayed

on the digital voltmeter was

equivalent to kilovolts.

Licensee

personnel

provided the inspector with the high

voltage probe technical

manual

which confirmed what the

technician

had stated.

The inspector noted that the digital

voltmeter was included in the licensee's

calibration -program

and

a calibration sticker

had. been attached

indicating that

it was within the calibration frequency.

The inspector

asked

about the calibration of the probe since

a calibration

sticker was absent.

Licensee

personnel

stated that the

probe did not receive

a calibration check

on site.

Furthermore,

vendor testing of the probe

was not acceptable

since the vendor did not have

a quality assurance

program

approved

by the licensee.

Failure to utilize a calibrated

high voltage measuring

device during the performance of

surveillance testing

on safety-related

equipment is contrary

to the requirements

of 10 CFR 50 Appendix

B Criterion XII

and is considered

to be

a violation.

Violation (400/94-13-03):

Failure to calibrate

high voltage

probe measuring

device.

Subsequent

to the inspector's

inquiry, licensee

personnel

verified the

1000 to

1 voltage divider of the probe

and

found it to be within manufacturer's

accuracy limits.

The inspectors

reviewed

NRC Information Notice 94-46,

Nonconservative

Reactor Coolant System

Leakage Calculation,

for its potential

impact

on the Harris plant.

The

information notice discussed

a problem identified at another

facility concerning

a nonconservatism

associated

with the

RCS unidentified leakage calculation required

by TS.

This

calculation

was performed considering total

volume changes

in various closed

system tanks; i.e., reactor coolant drain

tank, pressurizer relief tank,

volume control tank.

The

information notice stated that several

valve leakoff lines

associated

with the cold leg accumulators

in the safety

injection system drain into the

RCDT.

Since

RCS 'identified

leakage

was determined

by comparing

volume changes

in the

RCDT with changes

in the

VCT or the pressurizer,

additions

of non-RCS water to the

RCDT could falsely increase

the

identified leakage

value.

This inflated identified leakage

value would result in non-conservative

unidentified leakage

estimates

since unidentified leakage

was determined

by

subtracting

the identified leakrate

from total system

leakage.

The inspector

reviewed

system drawings

and procedure

OST-1026.

From this review, the inspector discovered that

valve stem leakoff lines from three safety injection system

cold leg accumulator discharge

isolation valves

(1SI-246,

247,

and 248),

and 1SI-354

and

353 in the low head

SI

system,

were connected

to the

RCDT.

Discussions with

licensee

personnel

indicated that

RCS leakage for the Harris

plant was calculated

in the

same

manner

as the subject plant

in the information notice.

The inspector

concluded that the

same potential

nonconservatism

existed for calculating

unidentified leakage

at Harris.

The inspector

reviewed data

for the current operating cycle and found that combined

unidentified

and identified leakage did not exceed

the

TS

limit for unidentified leakage.

The inspector

concluded

that

no immediate concern existed.

The inspector discussed

this issue with licensee

personnel

who issued

action item CAP-94H0454 to address

the potential

impact of non-RCS valve stem leakoff on

RCS leakage

calculations.

Engineering

Inspector

Followup Item (400/94-13-04):

Follow the

licensee's

activities to address

the impact of non-RCS valve

leakoff on

RCS leakage calculations.

Design, Installation

and Testing of Hodifications

(37551)

Plant

Change

Requests

(PCR) involving the installation of new or

modified systems

were reviewed to verify that the changes

were reviewed

and approved

in accordance

with 10 CFR 50.59, that the changes

were

performed in accordance

with technically adequate

and approved

procedures,

that subsequent

testing

and test results

met approved

acceptance

criteria or deviations

were resolved in an acceptable

manner,

and that appropriate

drawings

and facility procedures

were revised

as

necessary.

In addition,

PCRs documenting

engineering

evaluations

were

also reviewed.

The following modifications and/or testing in progress

was observed:

~ PCR-0420

RTD Bypass Elimination

~ PCR-5308

Safety Injection/Charging

Thermal Stratification

Evaluation

~ PCR-7339

Evaluation of OST-1214

CSIP Oil Cooler Flow Data

a ~

The inspectors

continued to review installation

and testing

documentation

associated

with PCR-0420.

As mentioned in NRC

Report 50-400/94-10,

the response

time testing for the resistance

temperature

detector

(RTD) instrument loop had

been

separated

into

three sections.

Sections

two and three collectively tested

the

response

time from the detector's

input to process

instrument

cabinets

PIC-1,

PIC-2,

and PIC-3, to the opening of the "A" and

"B" reactor trip breakers.

Those two sections

were performed

previously and verified by the inspectors

to meet acceptance

10

criteria.

Section

one of the instrument loop testing,

to

determine

the thermal

response

time of the newly installed

RTDs,

was reviewed during this inspection period.

Procedure

EST-300,

Reactor Trip Response

Time Evaluation,

documented

the testing for

the entire instrument loops

and included the results of the

thermal

response

time testing.

The inspector verified that each

of the

new

RTDs met the thermal

response

time acceptance

criteria

of less

than four seconds.

When the thermal

response

times were

added to the results of the circuit response,

reactor trip breaker

response,

and control rod gripper release

time tests

done

previously, the overall response

time of the

RTD loops

was within

the six seconds

assumed

in the

FSAR chapter

15 accident analysis.

In addition to

RTD response

time testing,

an

RCS hydrostatic test

was required

as

a result of the modification to reactor coolant

pressure

boundary piping.

This test

was conducted

on Nay 9 using

procedure

EPT-159,

ASME Section XI, Article IWB-5000 102 Percent

Hydrostatic Test.

During the test,

RCS pressure

was increased

from the normal operating

pressure

of 2235 psig to approximately

2290 psig,

and held there for four hours.

Licensee

personnel

then

performed

a visual examination of components within the

hydrostatic test

boundary in accordance

with procedure

EST-201,

ASHE System

Pressure

Tests.

The only deficiency noted during the

test

was

a small leak on

a quarter-inch

compression fitting near

valve

1RC-997.

A work ticket was initiated and the deficiency was

corrected

as required

by the procedure.

The inspectors

reviewed

completed

copies of both procedures

EPT-159

and

EST-201

and

concluded that this post modification testing for PCR-0420

was

conducted satisfactorily.

A final review of work tickets associated

with installing and

testing the

new

RTDs was conducted

by the inspectors

as well.

The

work tickets covered

implementation of PCR-0420 including the

demolition of the old

RTD bypass manifolds;

removal of main

control

room annunciators,

meters,

and switches;

determinating

and

reterminating of cables

outside the containment building;

and work

associated

with the

PIC cabinets.

The inspectors

concluded that

the overall

implementation of PCR-0420

was satisfactory.

On June

11 during the performance of procedure

OST-1214,

Emergency

Service water System Operability Train A, licensee

personnel

measured

emergency

service water flow to the CSIP oil coolers.

In

the normal

system valve alignment,

the

CSIP oil coolers receive

cooling water flow from both

ESW supply headers

through isolation

and check valves.

The return flowpath is through isolation valves

to each of the

ESW discharge

headers.

During the test,

one

ESW

header is idle with the

pump secured

and auxiliary reservoir

discharge

isolation valve closed.

Due to the absence

of installed

instrumentation,

a test rig consisting of a throttling valve,

venturi,

and strap-on flow detector

was utilized.

The test rig

was connected

to spare

one inch pipe instrument connections

located

downstream of the oil coolers.

Normal cooler return lines

11

were isolated to direct flow through the test rig.

The return

flowpath for the test rig was poly-tubing directed to a floor

drain.

Also pressure

indicators

were installed

on one inch drain

lines likewise located

downstream of the coolers.

As

a reference

point, pressure

data

was obtained during normal

system operation

through the coolers.

Utilizing the test rig, flow was throttled

in an attempt to recreate

normal

system operating

pressures.

The

actual

flow obtained

from this measurement

was 28.2

GPH for the

"B" CSIP coolers,

32.4

GPH for the

"C" CSIP coolers,

and 28.8

GPH

for the "A" CSIP coolers.

The licensee

had established

a limit of

30

GPH flow through these

coolers in the procedure to satisfy

technical

manual

recommendations.

Since both the "A" and

"B" CSIP

coolers did not pass sufficient flow the

pumps were declared

inoperable

and

an engineering

evaluation initiated.

A work

request

was written to inspect the "B" CSIP

sump lube oil cooler.

Inspection of this cooler revealed

no flow blockage.

Since the

"A" CSIP oil coolers

were inspected

during the recent refueling

outage,

these

coolers

were not reinspected.

Based

upon actual

data collected,

licensee

personnel

calculated

the headloss

of system piping and evaluated

the pressures

obtained

during the test.

The actual test

downstream

pressures

were

58

psig for the "A" CSIP

and

63 psig for the "B" CSIP

as

compared to

normal operating

pressures

of 40 psig.

Using the differential

pressures

actually measured

and the calculated

headloss

of system

piping,

a calculated

flowrate of over 60

GPM was determined to be

present

during normal

system operation

which greatly exceeded

the

30

GPM limit.

The licensee

concluded that sufficient flow was

available to support

pump operation.

The "B" CSIP was declared

operable.

The "A" CSIP remained

under

an equipment

clearance for

maintenance.

On June

27 procedure

OST 1215,

Emergency Service

Water System

Operability Train B, was performed which included

a revision to

utilize the calculations

performed for the opposite train test.

This test

was completed unsatisfactory

due to excessive

backpressure

present

downstream of the "A" CSIP oil cooler.

Attempts

by licensee

personnel

to depressurize

the idle

ESW return

header,

thereby reducing the backpressure

on the oil coolers,

were

unsuccessful.

Licensee

personnel

suspect

seat

leakage

past the

normal service water supply valve (ISW-39) to the "A" ESW supply

header.

The inspector

reviewed the licensee's

calculations

and inspected

the test rig utilized for the performance of the test.

The

inspector

also discussed

this situation with licensee

engineering

personnel.

Since the flow to the

CSIP oil coolers

was very

susceptible

to the backpressure

present

at the cooler outlet, the

inspector

asked licensee

personnel

to investigate

the potential

effect that

a single valve failure, consisting of an

ESW auxiliary

reservoir discharge

isolation valve

(1SW-270,

1SW-271) failing

closed,

might have

on CSIP cooling capability.

This failure might

12

produce similar backpressure

conditions

as to those

measured

during the test.

Presently

licensee

personnel

are reviewing the

system design

and are developing

a better method to measure

the

cooler flowrate.

Inspector

Followup Item (400/94-13-05):

Examine the licensee's

design

review of the

ESW system cooling water supply to the

CSIP

oil coolers

and development of a better test method.

On July

1 licensee

personnel split the cooling water flow return

from the

CSIP oil coolers

by closing the "A" CSIP oil cooler

return valve

(1SW-149) to the "B"

ESW discharge

header

and the "B"

CSIP oil cooler return valve

(1SW-170) to the "A" ESW discharge

header.

The "C" CSIP oil cooler return valve

(1SW-161) for the

"B"

ESW discharge

header

was also closed

since the

"C" CSIP was in

service replacing the out of service

"A" CSIP.

This system

configuration prevented

the potential single failure discussed

above from disabling all three

CSIPs.

Evaluation

PCR-5308

was performed to analyze

thermocouple

temperatures

measured

on safety injection,

normal charging

and

alternate

charging piping located

between

the

RCS loops

and the

first system

check valves.

Data from cycle four and cycle five

operations

was evaluated for thermal stratification

and cycling

effects.

The licensee

began monitoring this piping in response

to

NRC Bulletin 88-08,

Thermal

Stresses

in Piping Connected

to

Reactor Coolant Systems.

This matter

was previously reviewed in

NRC Inspection

Report 50-400/92-13

(IFI 400/90-10-04).

To check

for the existence of pipe flaws, licensee

personnel

had previously

non-destructively

examined the three cold leg injection and the

auxiliary charging lines in 1988.

No flaw indications were

identified at that time.

The monitoring program was established

to ensure

adverse

thermal stratification

and cycling conditions

did not occur.

The cycle four and cycle five data

was submitted to the licensee's

nuclear

steam

system supplier for analysis.

The analysis

was

completed

and transmitted to the licensee

on September

21,

1993.

This analysis

determined that several

valves exhibited -leakby with

resultant piping thermal stratification.

measured differential

temperatures

between

the top and bottom of piping consisted of the

following: 90 degrees

F for 1SI-81 (cold leg injection to loop 1),

150 degrees

F for 1SI-82 (cold leg injection loop 2),

90 degrees

F

for 1SI-83 (cold leg injection loop 3),

and

230 degrees

F for

valve

1CS-486 (alternate

charging line).

Data taken at two minute

intervals over

a 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> period was also evaluated

which indicated

that

no temperature

cycling was occurring.

The cycling of thermal stratification stresses

may lead to pipe

cracking.

Since there

was

no evidence that the temperatures

observed

were cycling, the analysis

concluded that the piping

structural integrity was not jeopardized.

However, the analysis

13

did contain several

recommendations

to ensure

continued

safe

operation.

The recommendations

included continued monitoring of

the piping, utilization of the alternate

charging flowpath as the

normal charging flowpath, repair of the valve seat

leakage,

and

non-destructive

examinations of affected welds near 'the

RCS loop

connections.

The licensee

repaired

valves

1CS-480

and 1SI-52 to

correct seat

leakage

through the alternate

charging line and cold

leg safety injection lines during the recent refueling outage.

In

addition, non-destructive

examinations

were performed

on the

affected welds.

No adverse

indications were identified.

The

licensee

does not plan to alter the normal charging flowpath.

No violations or deviations

were identified.

Plant Support

a ~

Plant Housekeeping

Conditions

(71707)

- Storage of material

and

components,

and cleanliness

conditions of various

areas

throughout

the facility were observed

to determine

whether safety and/or fire

hazards

existed.

b.

Radiological

Protection

Program

(71750)

- Radiation protection

control activities were observed

to verify that these activities

were in conformance with the facility policies

and procedures,

and

in compliance with regulatory requirements.

The inspectors

also

verified that selected

doors which controlled access

to very high

radiation areas

were appropriately locked.

Radiological postings

were likewise spot checked for adequacy.

The inspectors

noted

that progress

had

been

made in reducing the

amount of contaminated

areas

in the plant.

The "A" Residual

Heat

Removal

(RHR) heat

exchanger

and

pump rooms were decontaminated

during this

inspection period improving access

to these

areas.

(I)

The inspectors

reviewed the licensee's

activities for

controlling the specific activity in the spent fuel pools.

This issue

was previously reviewed in NRC Inspection

Reports

50 400/94 04)

93

16

93 02)

92 25)

92

12

92 04)

92 01)

91-22,

91-01,

and 90-21

by both the resident

inspectors

and

regional specialist

inspectors.

As mentioned

in

NRC

Inspection

Report 50-400/92-04,

the licensee

has

abandoned

the attempt to vacuum

up the cobalt

and iron particulates

(crud) from the bottom of the pools

and plans to leave the

crud

on the pool bottom for cleanup later after radioactive

decay.

Since it is not planed to utilize the

"D" spent fuel

pool for fuel storage until the year 2025, licensee

personnel

have

been using this pool

as

a repository for the

highly radioactive

crud which is transported

with the

boiling water reactor fuel assemblies

and settles

to the

bottom of the shipping casks.

In preparation for the annual

inspection of the spent fuel shipping cask,

licensee

personnel

pumped the crud which settled

on the bottom of the

cask to the

"D" pool.

The water in the

"D" pool is normally

segregated

from the other pools

and transfer canals

by

gates.

The inspector discussed

this matter with licensee

personnel

to review the fuel storage

design,

fuel pool cooling, fuel

pool inventory, potential

accident scenarios,

and determine

what precautions

had

been taken to control the crud.

The

inspector questioned

whether the activity within the pools

was still within the limits assumed

in the

FSAR (reference

NRC Inspection

Report 50-400/90-21, violation 400/90-21-04).

Although the

"C" and

"D" spent fuel pools

have cooling and

cleanup piping connected,

the construction of these

systems

has not been

completed

and therefore

these

systems

are not

available.

In addition, the

"C" and

"D" pools

have not been

racked to store

spent fuel.

Long term plans would include

plant modifications to provide these

components

and systems

prior to pool usage.

Temporary pipe caps

have

been

installed in piping connections

to the

"D" pool.

Blank

flanges or valves

seal

the end of unconnected

piping.

The

licensee

plans to install permanent

pipe covers

over the

pool connections this year under modification PCR-6414,

Fuel

Pool

C 5

D Seismic Evaluation.

The "A" and

"B" spent fuel

pools are connected

to

a fuel pool cooling and cleanup

system

and are intermittently operated

to provide cooling

and chemistry control.

Two separate

cooling systems

are

provided.

Piping connections

are located

near the top of

the pools

such that inadvertent

pipe ruptures

would not

uncover the spent fuel being stored.

Sections 3.8.3.6. 1.3

and 3.8.4. 1.3 of the

FSAR discuss

the qualifications of the

spent fuel pools

and the

FHB and state that they are

seismically designed

to withstand the effects of a safe

shutdown earthquake.

Sections

2.4. 12, 2.4. 13,

11. 1.7,

and 15.7.2 of the

FSAR

discuss

a potential

release

of spent fuel pool water through

a ruptured Refueling Water Storage

Tank

(RWST) to the site

environment.

Specific activity limits in Table

11. 1-7-1

ensure that in the event of this tank rupture, activity

concentrations

in surface water

and ground water would be

below the allowable concentrations

of 10 CFR 20.

Any spent

fuel pool leaks or leaks in connected

piping would be

contained within the seismically qualified

FHB or

WPB and

be

processed

accordingly before release offsite.

Since the

"C"

and

"D" pools are usually isolated

from the rest of the

pools,

a leak path from these

pools would most likely flow

to the

FHB.

Since the

FHB and spent fuel pools are

seismically qualified, failure of these structures

was not

considered

to be credible.

The evaluation

and calculations

for potential

accidents

were previously reviewed in

NRC

Inspection

Report 50-400/92-01.

15

In addition, Table

11. 1-7-1 also listed normal activity

levels which would limit general

area radiation levels to

less

than 2.5 mR/hr.

A review of radiation surveys

performed for these

areas

indicated general

area

dose rates

typically less

than

1 mR/hr at the walkways.

General

area

radiation dose rates

were approximately 2-3 mR/hr near the

"D" pool.

Underwater radiological

surveys of the

interconnecting

canals

indicated decreasing

radiation levels

as the spent fuel

was

moved from the north transfer

canal

through the main transfer

canal to the "A" and "B" pools.

This indicated that the crud was trickling off as the fuel

elements

were moved through the water

and

was mostly

deposited

in the north end of the canals.

Dose rates varied

from 21 R/hr at the bottom middle of the main transfer

canal

up to 621 R/hr in the north transfer

canal

where the

shipping cask basket

was flushed.

Dose rates

measured

at

the bottom of the

"D" pool indicated

a fairly uniform

distribution of crud over the pool bottom with an

approximate

20 R/hr radiation field.

Licensee

personnel

perform rotating weekly checks for pool

leakage

which is trended monthly.

The inspector

reviewed

these trends

and verified that only very slight leakage

has

been

noted thus far (less

than 0.5 gallons per month total

leakage

from all pools).

Routine radiological

surveys of

the

FHB operating floor are

done daily for general

area

radiation

and contamination.

In addition,

continuous

airborne activity devices

and general

area radiation devices

monitor these

areas.

The licensee's

control of items stored in the spent fuel

pools

was last inspected

in NRC Inspection

Report 50-400/91-

23.

The inspector

reviewed the licensee's

latest inventory

of these

items.

In addition to the crud, the licensee

has

stored

an underwater

pump in the

"D" pool.

Filters from

vacuuming the crud were presently stored in the north

transfer

canal

and were very radioactive.

A total of four

inventory items were temporarily stored in the

"C" and

"D"

pools.

Other than spent fuel

no items were stored in the

"A" or "B" pools.

The inspector toured the

FHB with

licensee

personnel

to identify the inventory items.

The inspector requested

to review the latest activity

samples of the pool

and canal water.

The licensee

had not

obtained

samples

from the areas of maximum crud deposition.

Although licensee

personnel

sample the "A" and "B" pools

and

the south transfer

canal

on

a monthly basis,

these

samples

are not representative

of crud concentrations

since these

samples

are taken from the water surface

and the crud has

typically settled to the bottom of the pools

and canals.

The results

from these

samples

were well below the

FSAR

limits.

No trends of the sample results

were available.

16

The licensee

was unable to quantify the present specific

activity in the fuel pools

and canals.

The limits imposed

by the

FSAR were calculated

assuming

the fuel pools were

filled to capacity

(7298 bundles)

and

an estimated

weight of

crud attached

to each

bundle which disperses

once the

assembly is moved.

The calculation also

assumed

that the

crud was homogeneously

mixed throughout the pools

and

canals.

Since the licensee

has only 1321 bundles presently

stored

in the pools,

the current specific activity levels

should

be within the limits specified in the

FSAR.

In

addition,

since the crud settles

to the bottom of the pools,

the inspector considered it unlikely that sufficient

quantities

would be released

during

a rupture of the

RWST

since piping connections

are located

near the top of the

pools.

The inspector concluded that the design of the spent fuel

pools

and cooling systems

was adequate

and that the licensee

was presently operating within the limits imposed

by the

FSAR.

Licensee

management

stated that

a review of crud

controls

was presently

underway

and that the quantification

of existing crud in the pools would be addressed.

Inspector

Followup Item (400/94-13-06):

Review the

licensee's

activities to quantify the

amount of crud in the

spent fuel pools.

The inspector

reviewed the

ALARA job briefings, radiological

surveys,

and interviewed involved health physics

personnel

in the last shipping cask

annual

inspection

in Hay 1994.

During handling of the first cask

and removal of the

internal basket,

approximately

746 millirem of personnel

exposure

was received

by plant personnel.

Teledosimetry

devices

were utilized to avoid exposures

due to direct

monitoring.

A shield wall, consisting of plastic

drums

filled with water,

was erected to create

a low dose

area

near the work area for both the workers

and health physics

personnel

monitoring the job. In addition,

a video tape of

this process

was taken

and reviewed prior to the handling of

the second

cask.

The inspector

watched the video.

Hovement

techniques

were reviewed

by licensee

personnel

and low dose

worker locations reestablished

to reduce

personnel

exposure.

Approximately 416 millirem of exposure

was received during

the second

basket

removal which indicated that the

licensee's

efforts were successful

in reducing the radiation

exposure.

Radiation levels

on the shipping casks

were approximately

2,000

R on contact.

During crud transfer

from the cask to

the

"D" spent fuel pool, general

area radiation levels rose

to approximately

10 mR/hr which decreased

as the crud slowly

settled to the bottom of the pool.

While crud was present

17

at the top of the pool, radiation dose rates

at the pool

surface

were approximately

75 mR/hr.

Security Control

(71750)

- The performance of various shifts of

the security force was observed

in the conduct of daily activities

which included:

protected

and vital area

access

controls;

searching of personnel,

packages,

and vehicles;

badge

issuance

and

retrieval; escorting of visitors; patrols;

and compensatory

posts.

In addition, the inspector

observed

the operational

status of

closed circuit television monitors, the intrusion detection

system

in the central

and secondary

alarm stations,

protected

area

lighting, protected

and vital area barrier integrity,

and the

security organization interface with operations

and maintenance.

Fire Protection

(71750)

- Fire protection activities, staffing and

equipment

were observed

to verify that fire brigade staffing was

appropriate

and that fire alarms,

extinguishing equipment,

actuating controls, fire fighting equipment,

emergency

equipment,

and fire barriers

were operable.

During plant tours,

areas

were

inspected

to ensure fire hazards

did not exist.

Emergency

Preparedness

(71750)

- Emergency

response facilities

were toured to verify availability for emergency operation.

Duty

rosters

were reviewed to verify appropriate staffing levels were

maintained.

As applicable,

emergency

preparedness

exercises

and

drills were observed to verify response

personnel

were adequately

trained.

On June

9,

1994, the inspector

observed

an emergency

preparedness

exercise

designed

to train one of the plant's four emergency

response

teams.

The objective of this exercise

was to demonstrate

for drill controllers/evaluators

that members of the control

room

staff and players stationed

in each of the three

emergency

response facilities could adequately

assess,

mitigate,

and report

accident conditions

as they progressed.

Several

attributes

were

tested

including communications

among

and between

response

facilities, provision of offsite dose

assessment,

and ability to

coordinate

and

augment

manpower

as

needed.

The inspector's

observations

throughout the exercise varied.

The

first three

hours of the scenario

were observed

from the Technical

Support Center.

Initially, command

and control of activities

by

the Site

Emergency Coordinator (lead person

in the

TSC) were weak.

The inspector

observed difficulties in establishing

phone

communications with other facilities, difficulties in finding

phone

numbers,

and

a delay in obtaining the status of an ongoing

repair activity (personnel

airlock door).

Finally, drill

briefings conducted

from the

TSC were not clear

and several

items

had to be repeated

due to audibility problems with the other

response

organizations.

18

The inspector also observed

the activities from the Operational

Support Center.

The inspector did not note

any deficiencies

in

prioritizing work activities,

but did observe

an example of

passiveness

concerning

one of the repair jobs.

When asked

by the

SEC about the status of the repairs

on the personnel

airlock door,

the

Damage Control Coordinator

responded

that

he didn't know

because

he hadn't

seen the auxiliary operators

return to the

operational

support center.

The inspector questioned

the status

of the efforts to fix the "A" CSIP breaker.

Several

personnel

in

the

OSC had to ask around before stating that attempts to replace

a control

power fuse were unsuccessful.

The inspector provided the above observations

to the emergency

preparedness

manager.

The inspector also reviewed

a draft of the

licensee's

own drill critique.

The critique contained

some of the

same

comments

noted

above including the difficulties in

establishing

phone communications

from the TSC,

and problems with

the drill briefings.

The critique did not identify some of the

other deficiencies

noted

above, specifically, the observations

from the

OSC.

The critique evaluated

the performance of the

OSC

as being satisfactory

and gave the

DCC credit for quickly

realizing the significance of the personnel

air lock release

path

and acting accordingly.

The inspector

acknowledged that the

June

9 exercise

was

a training scenario

designed to get

new

players qualified for the various

emergency

response

organization

positions.

However,

some of the above observations

involved

personnel

who had already

been qualified for their positions.

The

inspector did note that

command

and control in the

TSC improved

midway through the scenario

when the

SEC position was taken over

by the plant general

manager.

This was also noted in the

licensee's

critique.

At the close of the inspection period, the

licensee

was considering

plans to enhance

the emergency

response

organization

by relocating certain positions

among the response

facilities.

The inspectors

found plant housekeeping

and material condition of

components

to be satisfactory.

The licensee's

adherence

to radiological

controls, security controls, fire protection requirements,

emergency

preparedness

requirements

and

TS requirements

in these

areas

was

satisfactory.

No violations or deviations

were identified.

Review of Licensee

Event Reports

(92700)

The following Licensee

Event Report

was reviewed for potential generic

impact, to detect trends,

and to determine

whether corrective actions

appeared

appropriate.

As applicable,

events that were reported

immediately were reviewed

as they occurred to determine if the

TS were

satisfied.

LERs were reviewed in accordance

with the current

NRC

Enforcement Policy.

19

(Closed)

LER 93-04:

This

LER reported

a TS violation regarding

two

control

room ventilation system valves which had not been tested within

their required quarterly surveillance test intervals.

This matter

was

previously discussed

in

NRC Inspection

Report 50-400/94-05.

The

licensee

completed

implementation of PCR 7014, Correct

EBASCO Valve and

Damper Nomenclature

on Control

Room Switches,

the week of June

27,

1994.

The inspector

reviewed the implementation of this modification and

considered it satisfactory.

The valves affected

by the missed

surveillances

were given

new numbers

which are

now distinguishable

from

the dampers that were previously mistaken for them.

Exit Interview (30703)

The inspectors

met with licensee

representatives

(denoted in paragraph

1) at the conclusion of the inspection

on July 1,

1994.

During this

meeting,

the inspectors

summarized

the scope

and findings of the

inspection

as they are detailed in this report, with particular emphasis

on the Violations and Inspector

Follow-up Items addressed

below.

The

licensee

representatives

acknowledged

the inspector's

comments

and did

not identify as proprietary

any of the materials

provided to or reviewed

by the inspectors

during this inspection.

No dissenting

comments

from

the licensee

were received.

Item Number

Descri tion and Reference

400/94-13-01

400/94-13-02

400/94-13-03

400/94-13-04

400/94-13-05

400/94-13-06

Non-cited Violation:

Failure to maintain

configuration control for alternate miniflow valve

1CS-750,

paragraph

2.b.

Violation:

Failure to preplan

non-emergency

work on

valve

1SW-20,

paragraph

3.a(2).

Violation:

Failure to calibrate

high voltage probe

measuring

device,

paragraph

3.b(1).

Inspector

Followup Item:

Follow the licensee's

activities to address

the impact of non-RCS valve

leakoff on

RCS leakage calculations,

paragraph 3.b(2).

Inspector

Followup Item:

Examine the licensee's

design review of the

ESW system cooling water supply

to the CSIP oil coolers

and development of a better

test method,

paragraph

4.b.

Inspector

Followup Item:

Review the licensee's

activities to quantify the amount of crud in the spent

fuel pools,

paragraph

5.b(1).

Acronyms

and Initialisms

ACFR

-

Adverse Condition Feedback

Report

ALARA -

As

Low As Reasonably

Achievable

AO

ASNE

CFR

CSIP

DCC

EDG

EROS

ESW

FHB

FSAR

GPN

IFI

LER

mR

NRC

OSC

PIC

PCR

PSIG

RAB

RCDT

RCS

RHR

RTD

RWST

SI

TS

TSC

VCT

VDC

WPB

20

Auxiliary Operator

American Society of Hechanical

Engineers

Code of Federal

Regulations

Charging Safety Injection

Pump

Damage Control Coordinator

Emergency Diesel

Generator

Emergency

Response

Data System

Emergency Service Water

Fuel Handling Building

Final Safety Analysis Report

Gallons per Hinute

Inspector

Followup System

Licensee

Event Report

Niliroentgens

Nuclear Regulatory

Commission

Operational

Support Center

Process

Instrument Cabinet

Plant

Change

Request

Pounds

per Square

Inch Gage

Reactor Auxiliary Building

Reactor Coolant Drain Tank

Reactor Coolant System

Residual

Heat

Removal

Resistance

Temperature

Detector

Refueling Water Storage

Tank

Safety Injection

Technical Specification

Technical

Support Center

Volume Control Tank

Volts Direct Current

Waste Processing

Building