05000250/LER-1988-001, :on 880113,unit Experienced Turbine Runback Due to Dropped Control Rod Assembly & Manual Subcritical Reactor Trip Occurred When Addl Control Rods Dropped Into Core. Caused by Personnel Error.Personnel Counseled

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:on 880113,unit Experienced Turbine Runback Due to Dropped Control Rod Assembly & Manual Subcritical Reactor Trip Occurred When Addl Control Rods Dropped Into Core. Caused by Personnel Error.Personnel Counseled
ML17342B163
Person / Time
Site: Turkey Point NextEra Energy icon.png
Issue date: 02/12/1988
From: Hart R, Woody C
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF ADMINISTRATION & RESOURCES MANAGEMENT (ARM)
References
L-88-67, LER-88-001, LER-88-1, NUDOCS 8802170385
Download: ML17342B163 (8)


LER-1988-001, on 880113,unit Experienced Turbine Runback Due to Dropped Control Rod Assembly & Manual Subcritical Reactor Trip Occurred When Addl Control Rods Dropped Into Core. Caused by Personnel Error.Personnel Counseled
Event date:
Report date:
2501988001R00 - NRC Website

text

ACCESSION NBR F*C IL: 50-250 AUTH. NAME HART> R. D.

WOODYI C. O.

RECIP. NAME REGULA Y INFORMATION D ISTR IBUTI "YSTEM

( R IDS )

E 8802170385 DOC. DATE: 88/02/12 NOTARIZED:

NO DOCK,ET ¹ Turkey Point Plant1 Unit 31 Florida PoUjer and Light C

05000250 AUTHOR AFFILIATION Florida PoUJer 5 Light Co.

Florida Poojer 5 Light Co.

RECIPIENT AFFILIATION

SUBJECT:

LER 88-001-00: on 880113. unit experienced turbine runback due to dropped control rod assembly 8< manual subcritical T eactor trip occurred Nhen addi control rods dropped into core.

Caused bg personnel error. Personnel counseled.

W/880212 ltT.

DISTRIBUTION CODE:

IE22D COPIES RECEIVED: LTR i

ENCL I

SIZE:

TITLE:

50. 73 Licensee Event Repor t (LER) I Incident Rpt1 etc.

NOTES:

REC IP IENT ID CODE/NAME PD2-2 LA ED ISONI G COPIES LTTR ENCL 1

1 1.

RECIP IENT ID CODE/NAME PD2-2 PD COPIES LTTR ENCL 1

1 INTERNAL:

ACRS MICHFL SON AEQD/DOA AEOD/DSP/ROAB

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TOTAL NUMBER OF COPIES REQUIRED:

LTTR 46 ENCL 45

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NRC Form 366 (9 83)

LICENSEE EVENT REPORT (LER)

U.S. NUCLEAA REGULATORY COMMISSION APPROVED OMB NO. 31604104 EXPIRES: SI31ISS FACILITYNAME III DOCKET NUMBER 12)

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an Subcritical Reactor Trip When Additional Control Rods Dropped Into the Core EVENT DATE IS)

LER NUMBER (6I REPOR1'DATE(7)

OTHER FACILITIES INVOLVED(Sl MONTH OAY YEAR YEAR SSOVSNTIAL N VMS 6R: <4 REVISION NVMSSR MONTH OAY YEAR A

FACILITYNAMES DOCKET NUMBFRISI 0

5 0

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LICENSEE CONTACT FOR THIS LER (12I 50.73( ~ ) (2) (Ivl 50.73( ~)(2)(vl 60.73(el(2)(rill 50.73( ~)(2)(vill)(A) 50.73(eH2)

(vill)(BI 60.73( ~ )(2)(xI 0 THE REOUIREMENTS OF 10 CFR (): TCnrck onr or more ot tnr IoiroWinpl )11)

THIS REPORT IS SUBMITTED PURSUANT T 73.71(II) 73.71(cl OTHER ISprciiy In AOstrrct Oriow rnd In Trit, NRC Form 366AI NAME Randall D. Hart, Licensing Engineer TELEPHONE NUMBER AREA CODE 305 24 6 -

6 559 COMPLETE ONE I.INE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 113) n'v

CAUSE

SYSTEM COMPONENT MANUFAC.

TUAER REPORTABLE TO NPRDS

CAUSE

SYSTEM COMPONENT MANUFAC TURER EPORTABL'E TO NPADS A A C

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SUPPLEMENTAL REPORT EXPECTED (14)

YES (IIyes, compirte EXPECTED SUBMISSION DATE)

NO ABSTAACT I(.imit to )400 sprees, I.e., rpproximeteiy hftrrn sinrir specs typrrm'INn since) 118)

EXPECTED SUBMISSION DATE (15)

MONTH OAY YEAR On January 13, 1988, while at 100% power, Unit 3 experienced a turbine runback due to a dropped control rod assembly.

The operators commenced operating procedure (OP) 1604.1, Full Length RCC Periodic Exercise.

Step 8.4.1 was initiated to step shutdown bank A control rods, when rod control cluster (RCC) N-9 dropped into the core.

This energized the rod bottom bistable for N-9 initiating a rod position indication (RPI) turbine runback to approximately 70% power.

Off normal operating procedures were consulted to stabilize reactor power.

An attempt was made to retrieve the RCC which was unsuccessful.

The unit was shutdown to facilitate repairs.

During the shutdown sequence two more'CCs dropped and a manual reactor trip was initiated.

The unit was stabilized in mode 3.

An investigation into the root cause of the first dropped control rod determined that a pin on the connector for the movable gripper coil on the reactor head had been pushed out of engagement.

Therefore when the RCC was moved, the movable gripper coil did not engage and the RCC dropped into the core.

The other two dropped RCCs were due to personnel error in that a technician removed the power fuses to N-9 and did not identify that the power fuse to the movable gripper coil was common to two other RCCs.

The connector pins on the RCCs were inspected and engaged as necessary.

The appropriate personnel were counseled on this event.

NAC Form 366 (9 831 8802170385 880212 PDR ADDCK 05000250 8

PDR

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NRC Form 388A, (94)3)

LICENSEE NT REPORT ILER) TEXT CONTINU N

U.S. NUCLEAR REGULATORY COMMISSION APPROVEO OMB NO. 3150M)04 EXPIRES: 8/31/88 FACILITYNAME (1)

OOCKET NUMBER (2)

LER NUMBER (8)

YEAR

.'+8 SEQUENTIAL Po)r NN NUMSEII REVISION NUMS E II PAGE (3)

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1 0 00'2 OF EVENT:

On January 13, 1988, while at 100% power, Unit 3 experienced a turbine runback due to a dropped control rod assembly (EIIS:AA).

At 0407 on January 13,

1988, the operators commenced operating procedure (OP) 1604.1, Full Length RCC-Periodic Exercise.

Step 8.4.1 was initiated to step shutdown bank A control

rods, when rod control cluster (RCC) N-9 dropped into the core.

This energized the rod bottom bistable for N-9 initiating a rod position indication (RPI) turbine runback to approximately 70% power.

Off normal operating procedure (ONOP) 3-0NOP-089, Turbine Runback, was consulted to stabilize reactor power.

The Reactor Engineering Department was contacted for guidance and the recommendation was that if retrieval of the RCC was unsuccessful, reduce power to less than 50%.

At 0449, 3-0NOP-028, Reactor Control System Malfunction, was used in attempt to realign RCC N-9 with shutdown bank A.

This was unsuccessful and N-9 was declared inoperable.

At 0504 a unit load reduction to less than 50% reactor power was commenced.

An investigation by the Instrumentation and Control Department (I&C) determined that N-9 had an open circuit in the movable coil circuit.

At this time plant management decided to shutdown unit 3 to facilitate investigations.

The load reduction began at 0635 and the unit was taken off the line at 0737.

Further trouble shooting by I&C resulted in plant management deciding to shutdown the unit to cold shutdown (mode

5) to facilitate repairs.

At 1318, the shutdown of the unit was continued.

At 1319 with the D control rod bank at 100 steps, RCC M-10 (C control rod bank) dropped into the core.

This point corresponds to the 100 step overlap between the D and C control rod banks.

3-ONOP-028 was consulted for guidance and the reactor shutdown was continued.

At 1323, with the B control rod bank at 100 steps, RCC L-9 (A control rod bank) dropped into the core.

This point also corresponds to the 100 step overlap between control rod banks B and A.

At this point the operator manually tripped the reactor as required by 3-ONOP-028 due to the third RCC dropping into the core.

The unit was subsequently stabilized in mode 3 (hot standby).

CAUSE

OF EVENT:

An investigation into the root cause of the first dropped control rod determined that a pin on the connector for the movable gripper coil on the reactor head had been pushed partially out of engagement.

After time this pin became completely disengaged with the connector.

Therefore, when the operator attempted to move the RCC during the performance of OP 1604.8, the stationary coils disengaged from N-9, however, the movable coil did not engage on N-9 due to the pin in the connector not being engaged.

This resulted in the dropped RCC N-9.

The root cause for the partially engaged connector pin is still under investigation with the vendor.

During the shutdown, the connectors for the other RCCs were inspected for partially engaged connector pins and any discrepancies were corrected.

NRC FORM 3OSA (94)3)

<<U.S.GPO,1988 0 824 538/455

NRC Form 3EEA i (94)3)

LICENSEE NT REPORT (LER) TEXT CONTINU N

U.S. NUCLEAR REOULATORY COMMISSION APPROVED 0MB NO. 3150-0104 EXPIRES: 8/31/88 fACILITYNAME Ill DOCKET NUMBER 12)

VEAR LER NUMBER 16)

SEOVENTIAL NVMSER gi's REVISION NVMSEII PAOE 13)

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OF The root cause for the other two dropped RCCs was personnel error.

When RCC N-9 was taken out of service the power fuses to the stationary, lift and movable coils were pulled.

The technician removing the fuses used an uncontrolled label located on the power supply cabinet to guide his efforts and did not use controlled documents to verify that he was not affecting any other components when he removed the fuses.

The movable coils for RCCs N-9, M-10, and L-9 share a

common neutral fuse.

Therefore, when the power fuses for N-9 were

removed, the power to the movable coil for M-10 and L-9 was lost.

So when the RCC bank overlap initiated RCC movement, the movable coils for M-10 and L-9 did not energize and the RCCs dropped into the core.

ANALYSIS OP EVENT:

Upon initiation of the RPI rod bottom signal, a turbine runback was automatically initiated as designed.

Reactor coolant system (RCS) and secondary system parameters responded as expected for this type of event.

At the time of the reactor trip, Unit 3 was in mode 3 and in the process of inserting the control rod and shutdown banks into the core.

When the manual reactor trip signal was generated, the reactor trip breakers opened and shutdown and control rod banks inserted into the core as designed.

A post trip review was performed to assess the proper operation of safety-related equipment.

The post trip review established that the transient behavior of pertinent plant parameters for the reactor coolant system and steam generators responded as expected for a transient of this kind.

Based on the above, the health and safety of the public were not affected.

CORRECTIVE ACTIONS

1)

The connector pins for RCC N-9 were inspected and engaged properly.

The rest of the RCCs for Unit 3 were inspected for partially engaged connector pins.

Several partially engaged pins were found and corrected.

2)

The reason for the partially engaged pins is still under investigation.

Upon completion of this investigation, appropriate corrective actions will be taken.

3)

The I&C shop personnel have been counseled on the.cause of the multiple RCC drops and how to prevent future occurrences 4)

Trouble shooting procedures will be clarified to ensure that proper drawing and/or prints are consulted prior to fuse removal.

In this event a

noncontrolled label had been used to identify the fuses.

This label will be replaced.

NRC fORM SESA (94)3)

  • U.S.GPO;1986 0 62 ~ 538/455~

(94)3)

LICENSEE NT REPORT ILER) TEXT CONTINU N

U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMS ND. 3)50W104 EXPIRES; 8/31/68 FACILITYNAME (ll DOCKET NUMBER (2)

YEAR LER NUMBER (6) nW~'EOVENTIAL NO/

NVMSER Irido REVISION

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Upon approval of the post trip review and completion of required maintenance-activities, unit 3 will be returned to service.

6)

This event will be reviewed by the Training Department to determine if additional training is warranted.

ADDITIONALDETAILS:

The control rod system is supplied by Westinghouse.

Similar Occurrences:

LERs 251-85-021 and 251-86-002 reported events where a

turbine runback occurred due to a dropped control rod.

However, the root cause for those runbacks was different from this event.

NRC FOAM 366A 194)3) o U.S.GPO:1986 0 624 538/455

P. 0 14000, JUNO BEACH, FL 33408.0420 FfBRUARY 1 2 1988 L-88-67 10 CFR 50-73 U. S. Nuclear Regulatory Commission Attn:

Document Control Desk Washington, D.

C.

20555 Gentlemen:

Re:

Turkey Point Unit 3 Docket No. 50-250 Reportable Event:

88-01 Date of Event:

January 13, 1988 Turbine Runback Due to Dropped Control Rod and Subsequent Manual Subcritical Reactor Trip When The Additional Control Rods Dro ed Into the Core The attached Licensee Event Report (LER) is being submitted pursuant to the requirements of 10 CFR 50.73 to provide notification of the subject event.

Very truly yours, G4d g C.

O.

Execut ody e Vice President COW/SDF/gp Attachment cc:

Dr. J.

Nelson Grace, Regional Administrator, Region II, USNRC Senior Resident Inspector, USNRC, Turkey Point Plant SDF/012. LER

~8 i I an FPL Group company