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Category:LICENSEE EVENT REPORT (SEE ALSO AO RO)
MONTHYEAR05000250/LER-1999-001-02, :on 990623,manual RT from 100% Power Following Multiple Control Rod Drops Was Noted.Caused by Manual Action Taken by Reactor Control Operator.Inspected & Repaired Stationary Gripper Regulating Cards.With1999-07-20020 July 1999
- on 990623,manual RT from 100% Power Following Multiple Control Rod Drops Was Noted.Caused by Manual Action Taken by Reactor Control Operator.Inspected & Repaired Stationary Gripper Regulating Cards.With
05000250/LER-1998-007-02, :on 981020,containment Purge Supply,Valve Opened Wider than TS Limit.Caused by Improper Setting of Mechanical Stops.Incorporated Improved Standard Method of Measuring Angular Valve Position Into Sp.With1998-11-18018 November 1998
- on 981020,containment Purge Supply,Valve Opened Wider than TS Limit.Caused by Improper Setting of Mechanical Stops.Incorporated Improved Standard Method of Measuring Angular Valve Position Into Sp.With
05000250/LER-1998-006-02, :on 981006,unescorted Access Was Granted to Contractor Employee Who Falsified Background Info.Caused by Individual Who Knowingly Provided False Info.Denied Access to Individual on 981006.With1998-10-27027 October 1998
- on 981006,unescorted Access Was Granted to Contractor Employee Who Falsified Background Info.Caused by Individual Who Knowingly Provided False Info.Denied Access to Individual on 981006.With
05000250/LER-1998-004-02, :on 980921,automatic Reactor Trip Occurred. Caused by Inadequate re-correlation of Intermediate Range Neutron Flux Instrumentation Reactor Trip Bistable. Enhanced Applicable Plant Procedures.With1998-10-16016 October 1998
- on 980921,automatic Reactor Trip Occurred. Caused by Inadequate re-correlation of Intermediate Range Neutron Flux Instrumentation Reactor Trip Bistable. Enhanced Applicable Plant Procedures.With
05000250/LER-1998-005-02, :on 980924,suspended Safeguards During Severe Weather Due to Personnel Safety.Caused by Severe Weather Associated with Effects of Hurricane Georges.Fully Instituted Compensatory Measure.With1998-10-16016 October 1998
- on 980924,suspended Safeguards During Severe Weather Due to Personnel Safety.Caused by Severe Weather Associated with Effects of Hurricane Georges.Fully Instituted Compensatory Measure.With
05000250/LER-1998-003-02, :on 980619,discovered That Auxiliary Feedwater Sys Was Inoperable Due to Inadequate Inservice Testing of Valves.Caused by Misunderstanding of Testing Criteria.Util Revised Procedures & Verified Operability of Valves1998-07-15015 July 1998
- on 980619,discovered That Auxiliary Feedwater Sys Was Inoperable Due to Inadequate Inservice Testing of Valves.Caused by Misunderstanding of Testing Criteria.Util Revised Procedures & Verified Operability of Valves
05000250/LER-1997-007, :on 970730,automatic Reactor Trip Occurred Due to Closure of B Msiv.Caused by Failed BFD22S Relay.Six Relays on 3A,3B & 3C MSIVs Were Replaced & Implemented Plant Change to Disable Electronic Trip Function on 3 AFW Pumps1998-06-18018 June 1998
- on 970730,automatic Reactor Trip Occurred Due to Closure of B Msiv.Caused by Failed BFD22S Relay.Six Relays on 3A,3B & 3C MSIVs Were Replaced & Implemented Plant Change to Disable Electronic Trip Function on 3 AFW Pumps
05000250/LER-1998-002-02, :on 980513,discovered Potential LOCA-initiated Electrical Fault Which Places ECCS Outside Design Basis. Caused by Inadequate Review of Effect on non-safety Circuit failures.Re-powered PC-*-600A Relays1998-06-0909 June 1998
- on 980513,discovered Potential LOCA-initiated Electrical Fault Which Places ECCS Outside Design Basis. Caused by Inadequate Review of Effect on non-safety Circuit failures.Re-powered PC-*-600A Relays
05000250/LER-1997-009, :on 971114,discovered That CR Console Switch for 3B SGFP Was Not in Start Position.Caused by Inadequate Procedural Guidance.Revised Procedures 3/4-OP-074,informed Personnel of Event & Performed Walkdown of CR1998-03-24024 March 1998
- on 971114,discovered That CR Console Switch for 3B SGFP Was Not in Start Position.Caused by Inadequate Procedural Guidance.Revised Procedures 3/4-OP-074,informed Personnel of Event & Performed Walkdown of CR
05000250/LER-1998-001-02, :on 980216,manual Reactor Trip Occurred Due to Loss of Turbine Control Oil Pressure W/Steam Leak in Auxiliary Feedwater Steam Supply Piping.Auxiliary Governor Maint Instructions Will Be Revised1998-03-18018 March 1998
- on 980216,manual Reactor Trip Occurred Due to Loss of Turbine Control Oil Pressure W/Steam Leak in Auxiliary Feedwater Steam Supply Piping.Auxiliary Governor Maint Instructions Will Be Revised
05000250/LER-1997-008-01, :on 970909,containment Sump Debris Screens Outside Design Basis Due to Stress Damage Was Discovered. Caused by Inadequate Procedural Guidance & Personnel Error. Discrepancies Found on Screens Corrected1997-10-0808 October 1997
- on 970909,containment Sump Debris Screens Outside Design Basis Due to Stress Damage Was Discovered. Caused by Inadequate Procedural Guidance & Personnel Error. Discrepancies Found on Screens Corrected
05000250/LER-1997-006-02, :on 970722,manual Reactor Trip Occurred Due to Failed Rod Control Power Supplies.Replaced Twelve Power Supplies in Rod Control Logic & Power Cabinets1997-08-18018 August 1997
- on 970722,manual Reactor Trip Occurred Due to Failed Rod Control Power Supplies.Replaced Twelve Power Supplies in Rod Control Logic & Power Cabinets
05000250/LER-1997-005-01, :on 970618,RCP Oil Collection Sys Was Found Outside Design Basis.Caused Because Design Did Not Consider Component Parts to Be Potential Leakage Sources.Entire RCP Oil Collection Sys Was Reviewed1997-07-14014 July 1997
- on 970618,RCP Oil Collection Sys Was Found Outside Design Basis.Caused Because Design Did Not Consider Component Parts to Be Potential Leakage Sources.Entire RCP Oil Collection Sys Was Reviewed
05000251/LER-1997-002-02, :on 970423,automatic Reactor Tripped.Caused by Actuation of Turbine Overspeed Protection Circuit. Administrative Procedures Governing Inadequate Work Controls Will Be Revised to Capture Lessons Learned1997-05-22022 May 1997
- on 970423,automatic Reactor Tripped.Caused by Actuation of Turbine Overspeed Protection Circuit. Administrative Procedures Governing Inadequate Work Controls Will Be Revised to Capture Lessons Learned
05000250/LER-1997-003-01, :on 970410,mode Changed W/O Meeting Requirements of TS 3.0.4 Due to Inadequate Procedural Guidance.Night Order Was Issued to Inform Personnel That S/G Blowdown Keylock Switches Were Left in Drain1997-05-0909 May 1997
- on 970410,mode Changed W/O Meeting Requirements of TS 3.0.4 Due to Inadequate Procedural Guidance.Night Order Was Issued to Inform Personnel That S/G Blowdown Keylock Switches Were Left in Drain
05000250/LER-1997-004-01, :on 970411,auxiliary Feedwater Automatic Start Upon Trip of All Main Feedwater Pumps,Occurred.Caused by Mispositioned Valve Closing.Valves Listed as Inappropriately Positioned Were Repositioned1997-05-0909 May 1997
- on 970411,auxiliary Feedwater Automatic Start Upon Trip of All Main Feedwater Pumps,Occurred.Caused by Mispositioned Valve Closing.Valves Listed as Inappropriately Positioned Were Repositioned
05000251/LER-1997-001-02, :on 970327,ECCS Recirculation Loop Leakage Was Found to Be in Condition Outside Design Basis Due to Gasket Movement During Installation During Spring 1966 Reassembly. Gasket Replaced & Pump Tested1997-04-25025 April 1997
- on 970327,ECCS Recirculation Loop Leakage Was Found to Be in Condition Outside Design Basis Due to Gasket Movement During Installation During Spring 1966 Reassembly. Gasket Replaced & Pump Tested
05000250/LER-1997-002-01, :on 970303,manual Reactor Trip Following Rod Control Urgent Failure Alarm Occurred.Caused by Phase Failure Detection on Stationary a Circuits of 2BD Rod Control Cabinet.Air Conditioning Replaced1997-03-28028 March 1997
- on 970303,manual Reactor Trip Following Rod Control Urgent Failure Alarm Occurred.Caused by Phase Failure Detection on Stationary a Circuits of 2BD Rod Control Cabinet.Air Conditioning Replaced
05000250/LER-1997-001-01, :on 970118,missed Surveillance on CR Position Verification Occurred Due to Inoperable Rod Deviation Monitor.Faulty Circuit Common Connection Was Corrected & Rdm Operability Was Restored1997-03-26026 March 1997
- on 970118,missed Surveillance on CR Position Verification Occurred Due to Inoperable Rod Deviation Monitor.Faulty Circuit Common Connection Was Corrected & Rdm Operability Was Restored
05000250/LER-1996-004, :on 970107,identified Three Instances of Inadequate Surveillance Testing.Caused by Inadequate Surveillance Procedures.Surveillance Procedures Revised1997-02-0303 February 1997
- on 970107,identified Three Instances of Inadequate Surveillance Testing.Caused by Inadequate Surveillance Procedures.Surveillance Procedures Revised
05000250/LER-1996-012-01, :on 961204,determined Containment Average Temp Being Determined Based on Only Two Temp Elements Instead of Three as Required by Tss.Caused by Log Only Requiring One Entry.Log Revised1996-12-27027 December 1996
- on 961204,determined Containment Average Temp Being Determined Based on Only Two Temp Elements Instead of Three as Required by Tss.Caused by Log Only Requiring One Entry.Log Revised
05000250/LER-1996-011-01, :on 961009,potential for Overpressurizing Post Accident Containment Vent Filter Housings Occurred.Caused by Improper Change Mgt.Monitoring Sys Operating Procedures Revised1996-11-0606 November 1996
- on 961009,potential for Overpressurizing Post Accident Containment Vent Filter Housings Occurred.Caused by Improper Change Mgt.Monitoring Sys Operating Procedures Revised
05000250/LER-1996-010-01, :on 960924,manual Reactor Shutdown Occurred. Caused by Failed Rod Control Sys Regulation Card in 2AC Power cabinet.2AC Power Cabinet DC Power Supplies,Cabling & Connectors Checked1996-10-22022 October 1996
- on 960924,manual Reactor Shutdown Occurred. Caused by Failed Rod Control Sys Regulation Card in 2AC Power cabinet.2AC Power Cabinet DC Power Supplies,Cabling & Connectors Checked
05000250/LER-1996-009-01, :on 960729,failed to Reflect Heavy Load Design Info in Procedural Controls.Caused by Failure to Incorporate 1982 Procedure Changes.Suspended Lifting of Heavy Loads & Took Turbine Bldg Crane OOS1996-08-27027 August 1996
- on 960729,failed to Reflect Heavy Load Design Info in Procedural Controls.Caused by Failure to Incorporate 1982 Procedure Changes.Suspended Lifting of Heavy Loads & Took Turbine Bldg Crane OOS
05000250/LER-1996-008, :on 960521,surveillance Method for Testing Emergency Diesel Generators (EDG) Determined Inadequate. Caused by Personnel Error.All Four EDGs Rapid Start Tested & EDG Surveillance Procedures Modified1996-06-18018 June 1996
- on 960521,surveillance Method for Testing Emergency Diesel Generators (EDG) Determined Inadequate. Caused by Personnel Error.All Four EDGs Rapid Start Tested & EDG Surveillance Procedures Modified
05000251/LER-1996-001-03, :on 960409,manual RT Occurred Due to Turbine Governer Control Oil Perturbation.Disassembled & Inspected Governor Valve for Cleanliness & Corrosion Products1996-05-0606 May 1996
- on 960409,manual RT Occurred Due to Turbine Governer Control Oil Perturbation.Disassembled & Inspected Governor Valve for Cleanliness & Corrosion Products
05000250/LER-1996-007, :on 960329,inadvertent ESF Actuation Occurred During Refueling Outage Due to Cognitive Personnel Error. Personnel Involved Counseled & Integrated Safeguards Test Procedures Being Revised1996-04-29029 April 1996
- on 960329,inadvertent ESF Actuation Occurred During Refueling Outage Due to Cognitive Personnel Error. Personnel Involved Counseled & Integrated Safeguards Test Procedures Being Revised
05000250/LER-1996-006, :on 960327,manual RT Occurred Due to 3C Transformer Lockout & Loss of 3B SG Mfp.Replaced SAM Timer Relay in 3AC161996-04-25025 April 1996
- on 960327,manual RT Occurred Due to 3C Transformer Lockout & Loss of 3B SG Mfp.Replaced SAM Timer Relay in 3AC16
05000250/LER-1996-005, :on 960326,certain Safety Injection Accumulator Filled Evolutions Resulted in cross-tied Configuration.C/A: Night Order Written & Operations Procedure 3/4-OP-064 Revised1996-04-23023 April 1996
- on 960326,certain Safety Injection Accumulator Filled Evolutions Resulted in cross-tied Configuration.C/A: Night Order Written & Operations Procedure 3/4-OP-064 Revised
05000250/LER-1996-003, :on 960222,two Arpi Inoperable & TS 3.0.3 Entered.Proposed License Amend Submitted to Revise Allowed Misalignment from +/-12 Steps to =/-18 Steps Between Arpi & Dpi at Less than 90% Power1996-03-18018 March 1996
- on 960222,two Arpi Inoperable & TS 3.0.3 Entered.Proposed License Amend Submitted to Revise Allowed Misalignment from +/-12 Steps to =/-18 Steps Between Arpi & Dpi at Less than 90% Power
05000250/LER-1996-002, :on 960209,automatic Turbine Trip/Rt Occurred Due to High SG Level.Caused by Personnel Error.Replaced Both Hinge Pins on B SGFP Discharge Check Valve1996-03-0606 March 1996
- on 960209,automatic Turbine Trip/Rt Occurred Due to High SG Level.Caused by Personnel Error.Replaced Both Hinge Pins on B SGFP Discharge Check Valve
05000250/LER-1996-001, :on 960131,intake CWS Flow Rates Found W/ Potential to Be Less than Required by Design Basis.Caused by Influx of Aquatic Grass & Algae Onto Basket Strainers of Icw Flow Path.Mechanically Cleaned Strainers1996-03-0101 March 1996
- on 960131,intake CWS Flow Rates Found W/ Potential to Be Less than Required by Design Basis.Caused by Influx of Aquatic Grass & Algae Onto Basket Strainers of Icw Flow Path.Mechanically Cleaned Strainers
05000250/LER-1995-007-01, :on 951017,manual RT Occurred Following Drop of Four Control Rods.Caused by Water Intrusion Into Rod Control Power Cabinet 2BD.Inspected Control Power Cabinet 2BD for Other Water Damage1995-11-0909 November 1995
- on 951017,manual RT Occurred Following Drop of Four Control Rods.Caused by Water Intrusion Into Rod Control Power Cabinet 2BD.Inspected Control Power Cabinet 2BD for Other Water Damage
05000250/LER-1995-006-01, :on 950913,analysis Showed That CCW Exchangers Susceptible to Damage Due to flow-induced Vibration.Ccw Sys Has Been Flow Balanced to Closer Tolerances1995-10-12012 October 1995
- on 950913,analysis Showed That CCW Exchangers Susceptible to Damage Due to flow-induced Vibration.Ccw Sys Has Been Flow Balanced to Closer Tolerances
05000250/LER-1995-005-01, :on 950818,containment Pressure Testing Procedure Resulted in Inhibiting Both Trains of Containment Pressure from Initiated Esf.Revised Procedure to Require Testing of Each Train Separately1995-09-13013 September 1995
- on 950818,containment Pressure Testing Procedure Resulted in Inhibiting Both Trains of Containment Pressure from Initiated Esf.Revised Procedure to Require Testing of Each Train Separately
05000250/LER-1994-005, :on 941103,both Units Outside Design Basis Due to Design Defect in Safeguards Bus Sequencer Test Logic. Resumed Monthly Manual Testing of Sequencer1995-07-17017 July 1995
- on 941103,both Units Outside Design Basis Due to Design Defect in Safeguards Bus Sequencer Test Logic. Resumed Monthly Manual Testing of Sequencer
05000250/LER-1995-004, :on 950407,unit Being Shutdown to Investigate Recurring non-urgent Failure Alarms from Redundant Rod Control Power Supplies.Reactor Manually Tripped.All Four PS-3 Power Supplies Replaced1995-05-0505 May 1995
- on 950407,unit Being Shutdown to Investigate Recurring non-urgent Failure Alarms from Redundant Rod Control Power Supplies.Reactor Manually Tripped.All Four PS-3 Power Supplies Replaced
05000250/LER-1995-003, :on 950309,intake Cooling Water Flow Rate Through CCW Heat Exchangers Fell Below Assumed Design Basis. Caused by an Influx of Aquatic Grass & Algae Onto Basket Strainers.Strainers Cleaned1995-04-0707 April 1995
- on 950309,intake Cooling Water Flow Rate Through CCW Heat Exchangers Fell Below Assumed Design Basis. Caused by an Influx of Aquatic Grass & Algae Onto Basket Strainers.Strainers Cleaned
05000250/LER-1995-002, :on 950215,inadequate Definition of Loops Filled Resulted in Units in Condition Prohibited by Ts. Issued TS Position Statement to Define Term Loops Filled as Used in TS 6.4.1.1.41995-03-13013 March 1995
- on 950215,inadequate Definition of Loops Filled Resulted in Units in Condition Prohibited by Ts. Issued TS Position Statement to Define Term Loops Filled as Used in TS 6.4.1.1.4
05000250/LER-1994-006-03, :on 941226,C Main Feedwater Control Valve Failed Closed,Causing Reactor & Turbine Trips.Caused by Loose Screw Terminal Connection.I/P Transducers Replaced W/ New Model W/Different Design Wire Connection1995-01-20020 January 1995
- on 941226,C Main Feedwater Control Valve Failed Closed,Causing Reactor & Turbine Trips.Caused by Loose Screw Terminal Connection.I/P Transducers Replaced W/ New Model W/Different Design Wire Connection
05000251/LER-1994-006-02, :on 941130,Unit 4 Tripped Automatically.Caused by Failure of Flexible Link Connection Between Main Generator B Phase Bus & Associated Isolated Phase Bus Bar. All Bolts on Flexible Link Checked1994-12-13013 December 1994
- on 941130,Unit 4 Tripped Automatically.Caused by Failure of Flexible Link Connection Between Main Generator B Phase Bus & Associated Isolated Phase Bus Bar. All Bolts on Flexible Link Checked
05000250/LER-1994-004-03, :on 941103,Unit 3 Outside Design Basis Due to Two of Three Required Safety Injection Pumps Inoperable. Control Switches for 3A & 3B Safety Injection Pumps Immediately Returned to Automatic1994-11-10010 November 1994
- on 941103,Unit 3 Outside Design Basis Due to Two of Three Required Safety Injection Pumps Inoperable. Control Switches for 3A & 3B Safety Injection Pumps Immediately Returned to Automatic
05000250/LER-1994-005-03, :on 941103,design Defect in Safeguards Bus Sequencer Test Logic Places Both Units Outside Design Basis. Caused by 3A Sequencer Failed to Respond as Expected to Opposite Unit SI Signal1994-11-10010 November 1994
- on 941103,design Defect in Safeguards Bus Sequencer Test Logic Places Both Units Outside Design Basis. Caused by 3A Sequencer Failed to Respond as Expected to Opposite Unit SI Signal
05000251/LER-1994-004-02, :on 940923,Unit 4 Tripped Automatically from Rated Power.Caused by Faulty Regulator Transistor.Faulty Backup Power Supply Replaced & Maint History for Power Supplies Reviewed1994-10-21021 October 1994
- on 940923,Unit 4 Tripped Automatically from Rated Power.Caused by Faulty Regulator Transistor.Faulty Backup Power Supply Replaced & Maint History for Power Supplies Reviewed
05000251/LER-1994-005-02, :on 940924,Unit 4 Manually Tripped.Caused by Manual Actuation.Light Bulb & Socket Replaced1994-10-20020 October 1994
- on 940924,Unit 4 Manually Tripped.Caused by Manual Actuation.Light Bulb & Socket Replaced
05000250/LER-1994-003-03, :on 940720 & 21,util Discovered That Several Required Valve Stroke Time Surveillances Had Not Been Performed.Caused by Personnel Error.Personnel Reassigned & Procedures and Surveillance Tracking Software Enhanced1994-08-16016 August 1994
- on 940720 & 21,util Discovered That Several Required Valve Stroke Time Surveillances Had Not Been Performed.Caused by Personnel Error.Personnel Reassigned & Procedures and Surveillance Tracking Software Enhanced
05000250/LER-1994-001, :on 940119,three Surveillance Failures Were Caused by Failure of Solenoids to Change Position When de-energized.Changed Solenoid Valves from de-energize to Actuate to Energize to Actuate Configuration1994-07-26026 July 1994
- on 940119,three Surveillance Failures Were Caused by Failure of Solenoids to Change Position When de-energized.Changed Solenoid Valves from de-energize to Actuate to Energize to Actuate Configuration
05000250/LER-1994-002-03, :on 940505,spurious Actuation of 3A Safety Injection Signal Occurred.Caused by Intermittent seal-in Contact Failure of Block relay.SIB-1 Relay Was Replaced & System Tested to Demonstrate Operability1994-05-31031 May 1994
- on 940505,spurious Actuation of 3A Safety Injection Signal Occurred.Caused by Intermittent seal-in Contact Failure of Block relay.SIB-1 Relay Was Replaced & System Tested to Demonstrate Operability
05000251/LER-1994-003, :on 940318,ARPI Indicated Greater than Twelve Steps Deviation from Associated Group Counter.Caused by Rod Position Indication Varying W/Temp.Apris Adjusted.W/1994-04-11011 April 1994
- on 940318,ARPI Indicated Greater than Twelve Steps Deviation from Associated Group Counter.Caused by Rod Position Indication Varying W/Temp.Apris Adjusted.W/
05000251/LER-1994-002-01, :on 940310,personnel Discovered Indication of Boric Acid on a Flux Mapper Guide Tube.Caused by Tgscc. Plant Shut Down & Leaking Guide Tube Repaired1994-04-0101 April 1994
- on 940310,personnel Discovered Indication of Boric Acid on a Flux Mapper Guide Tube.Caused by Tgscc. Plant Shut Down & Leaking Guide Tube Repaired
1999-07-20
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML20217L9371999-10-20020 October 1999 Safety Evaluation Supporting Licensee Proposed Alternative from Certain Requirements of ASME Code,Section XI for First 10-Yr Interval Request for Relief for Containment Inservice Insp Program L-99-221, Monthly Operating Repts for Sept 1999 for Turkey Point,Units 3 & 4.With1999-09-30030 September 1999 Monthly Operating Repts for Sept 1999 for Turkey Point,Units 3 & 4.With L-99-202, Monthly Operating Repts for Aug 1999 for Turkey Point,Units 3 & 4.With1999-08-31031 August 1999 Monthly Operating Repts for Aug 1999 for Turkey Point,Units 3 & 4.With L-99-179, Monthly Operating Repts for July 1999 for Turkey Point,Units 3 & 4.With1999-07-31031 July 1999 Monthly Operating Repts for July 1999 for Turkey Point,Units 3 & 4.With 05000250/LER-1999-001-02, :on 990623,manual RT from 100% Power Following Multiple Control Rod Drops Was Noted.Caused by Manual Action Taken by Reactor Control Operator.Inspected & Repaired Stationary Gripper Regulating Cards.With1999-07-20020 July 1999
- on 990623,manual RT from 100% Power Following Multiple Control Rod Drops Was Noted.Caused by Manual Action Taken by Reactor Control Operator.Inspected & Repaired Stationary Gripper Regulating Cards.With
L-99-163, Monthly Operating Repts for June 1999 for Turkey Point,Units 3 & 4.With1999-06-30030 June 1999 Monthly Operating Repts for June 1999 for Turkey Point,Units 3 & 4.With ML17355A3681999-06-30030 June 1999 Revised Update to Topical QA Rept, Dtd June 1999 ML17355A3611999-06-30030 June 1999 Refueling Outage ISI Rept L-99-134, Monthly Operating Repts for May 1999 for Turkey Point,Units 3 & 4.With1999-05-31031 May 1999 Monthly Operating Repts for May 1999 for Turkey Point,Units 3 & 4.With ML17355A3291999-05-0505 May 1999 Revised SE Supporting Evaluation for Certain Fire Zones in Tubine Building at Plant,Units 3 & 4 & Granting Licensee Request for Exemption from Technical Requirements of Section III.G.2a ML17355A3221999-05-0505 May 1999 Safety Evaluation Supporting Amends 200 & 194 to Licenses DPR-31 & DPR-41,respectively ML20217B9871999-04-0808 April 1999 Changes,Tests & Experiments Made as Allowed by 10CFR50.59 for Period Covering 971014-990408 ML17355A2881999-04-0505 April 1999 COLR for Turkey Point Unit 4 Cycle 18 L-99-087, Monthly Operating Repts for Mar 1999 for Turkey Point,Units 3 & 4.With1999-03-31031 March 1999 Monthly Operating Repts for Mar 1999 for Turkey Point,Units 3 & 4.With ML17355A2791999-03-26026 March 1999 Safety Evaluation Concluding That No Outstanding Ampacity Derating Issues as Identified in GL 92-08 for Plants L-99-063, Monthly Operating Repts for Feb 1999 for Turkey Point Nuclear Power Plant,Units 3 & 4.With1999-02-28028 February 1999 Monthly Operating Repts for Feb 1999 for Turkey Point Nuclear Power Plant,Units 3 & 4.With ML17355A2161999-02-0303 February 1999 Safety Evaluation Supporting Amends 199 & 193 to Licenses DPR-31 & DPR-41,respectively L-99-033, Monthly Operating Repts for Jan 1999 for Turkey Point,Units 3 & 4.With1999-01-31031 January 1999 Monthly Operating Repts for Jan 1999 for Turkey Point,Units 3 & 4.With ML17355A2201999-01-20020 January 1999 Refueling Outage ISI Rept L-99-004, Monthly Operating Repts for Dec 1998 for Turkey Point,Units 3 & 4.With1998-12-31031 December 1998 Monthly Operating Repts for Dec 1998 for Turkey Point,Units 3 & 4.With L-98-297, Monthly Operating Repts for Nov 1998 for Turkey Point,Units 3 & 4.With1998-11-30030 November 1998 Monthly Operating Repts for Nov 1998 for Turkey Point,Units 3 & 4.With 05000250/LER-1998-007-02, :on 981020,containment Purge Supply,Valve Opened Wider than TS Limit.Caused by Improper Setting of Mechanical Stops.Incorporated Improved Standard Method of Measuring Angular Valve Position Into Sp.With1998-11-18018 November 1998
- on 981020,containment Purge Supply,Valve Opened Wider than TS Limit.Caused by Improper Setting of Mechanical Stops.Incorporated Improved Standard Method of Measuring Angular Valve Position Into Sp.With
ML17354B1891998-11-0909 November 1998 Simulatory Certification Update 2 L-98-281, Monthly Operating Repts for Oct 1998 for Turkey Point,Units 3 & 4.With1998-10-31031 October 1998 Monthly Operating Repts for Oct 1998 for Turkey Point,Units 3 & 4.With 05000250/LER-1998-006-02, :on 981006,unescorted Access Was Granted to Contractor Employee Who Falsified Background Info.Caused by Individual Who Knowingly Provided False Info.Denied Access to Individual on 981006.With1998-10-27027 October 1998
- on 981006,unescorted Access Was Granted to Contractor Employee Who Falsified Background Info.Caused by Individual Who Knowingly Provided False Info.Denied Access to Individual on 981006.With
ML17354B1591998-10-23023 October 1998 COLR for Turkey Point Unit 3 Cycle 17 05000250/LER-1998-005-02, :on 980924,suspended Safeguards During Severe Weather Due to Personnel Safety.Caused by Severe Weather Associated with Effects of Hurricane Georges.Fully Instituted Compensatory Measure.With1998-10-16016 October 1998
- on 980924,suspended Safeguards During Severe Weather Due to Personnel Safety.Caused by Severe Weather Associated with Effects of Hurricane Georges.Fully Instituted Compensatory Measure.With
05000250/LER-1998-004-02, :on 980921,automatic Reactor Trip Occurred. Caused by Inadequate re-correlation of Intermediate Range Neutron Flux Instrumentation Reactor Trip Bistable. Enhanced Applicable Plant Procedures.With1998-10-16016 October 1998
- on 980921,automatic Reactor Trip Occurred. Caused by Inadequate re-correlation of Intermediate Range Neutron Flux Instrumentation Reactor Trip Bistable. Enhanced Applicable Plant Procedures.With
L-98-262, Monthly Operating Repts for Sept 1998 for Turkey Point Unit 3 & 4.With1998-09-30030 September 1998 Monthly Operating Repts for Sept 1998 for Turkey Point Unit 3 & 4.With ML17354B1021998-09-14014 September 1998 Correction to SER Page 5 of SE & Page 6 of Ineel Technical Ltr Rept to Reflect Change of Word Then with Also, Submitted on 980817 in Response to Util 980409 Request Relief from Certain Requirements of ASME Code,Section XI ML17354B0971998-09-0909 September 1998 Part 21 Rept Re Possible Machining Defect in Certain One Inch Stainless Steel Swagelok Front Ferrules,Part Number SS-1613-1.Caused by Tubing Slipping Out of Fitting at Three Times Working Pressure of Tubing.Notified Affected Utils L-98-236, Monthly Operating Repts for Aug 1998 for Turkey Points,Units 3 & 4.With1998-08-31031 August 1998 Monthly Operating Repts for Aug 1998 for Turkey Points,Units 3 & 4.With ML17354B0901998-08-17017 August 1998 SER Accepting Revised Requests for Relief Numbers 11 & 18 for Turkey Point,Units 3 & 4 L-98-206, Monthly Operating Repts for July 1998 for Turkey Point,Units 3 & 41998-07-31031 July 1998 Monthly Operating Repts for July 1998 for Turkey Point,Units 3 & 4 ML17354B0541998-07-16016 July 1998 SER Accepting Alternative Proposed by Licensee in That Revising FSAR 6 Months After Refueling Outages for Each Unit Not Necessary to Achieve Underlying Purpose of Rule (10CFR50.71(e)(4)) 05000250/LER-1998-003-02, :on 980619,discovered That Auxiliary Feedwater Sys Was Inoperable Due to Inadequate Inservice Testing of Valves.Caused by Misunderstanding of Testing Criteria.Util Revised Procedures & Verified Operability of Valves1998-07-15015 July 1998
- on 980619,discovered That Auxiliary Feedwater Sys Was Inoperable Due to Inadequate Inservice Testing of Valves.Caused by Misunderstanding of Testing Criteria.Util Revised Procedures & Verified Operability of Valves
ML17354B0421998-07-0909 July 1998 Safety Evaluation Supporting Amends 198 & 192 to Licenses DPR-31 & DPR-41,respectively L-98-187, Monthly Operating Repts for June 1998 for Turkey Point,Units 3 & 41998-06-30030 June 1998 Monthly Operating Repts for June 1998 for Turkey Point,Units 3 & 4 ML17354B0171998-06-29029 June 1998 Rev 1 to PTN-FPER-97-013, Evaluation of Turbine Lube Oil Fire 05000250/LER-1997-007, :on 970730,automatic Reactor Trip Occurred Due to Closure of B Msiv.Caused by Failed BFD22S Relay.Six Relays on 3A,3B & 3C MSIVs Were Replaced & Implemented Plant Change to Disable Electronic Trip Function on 3 AFW Pumps1998-06-18018 June 1998
- on 970730,automatic Reactor Trip Occurred Due to Closure of B Msiv.Caused by Failed BFD22S Relay.Six Relays on 3A,3B & 3C MSIVs Were Replaced & Implemented Plant Change to Disable Electronic Trip Function on 3 AFW Pumps
ML17354A9651998-06-0909 June 1998 Safety Evaluation Supporting Amends 197 & 191 to Licenses DPR-31 & DPR-41,respectively 05000250/LER-1998-002-02, :on 980513,discovered Potential LOCA-initiated Electrical Fault Which Places ECCS Outside Design Basis. Caused by Inadequate Review of Effect on non-safety Circuit failures.Re-powered PC-*-600A Relays1998-06-0909 June 1998
- on 980513,discovered Potential LOCA-initiated Electrical Fault Which Places ECCS Outside Design Basis. Caused by Inadequate Review of Effect on non-safety Circuit failures.Re-powered PC-*-600A Relays
L-98-163, Monthly Operating Repts for Turkey Point,Units 3 & 41998-05-31031 May 1998 Monthly Operating Repts for Turkey Point,Units 3 & 4 ML20248F7441998-05-31031 May 1998 Reactor Vessel Working Group,Response to RAI Regarding Reactor Pressure Vessel Integrity ML17354A9351998-05-12012 May 1998 Safety Evaluation Supporting Amends 196 & 190 to Licenses DPR-31 & DPR-41,respectively L-98-128, Monthly Operating Repts for Apr 1998 for Turkey Point,Units 3 & 41998-04-30030 April 1998 Monthly Operating Repts for Apr 1998 for Turkey Point,Units 3 & 4 L-98-095, Monthly Operating Repts for Mar 1998 for Turkey Point,Units 3 & 41998-03-31031 March 1998 Monthly Operating Repts for Mar 1998 for Turkey Point,Units 3 & 4 05000250/LER-1997-009, :on 971114,discovered That CR Console Switch for 3B SGFP Was Not in Start Position.Caused by Inadequate Procedural Guidance.Revised Procedures 3/4-OP-074,informed Personnel of Event & Performed Walkdown of CR1998-03-24024 March 1998
- on 971114,discovered That CR Console Switch for 3B SGFP Was Not in Start Position.Caused by Inadequate Procedural Guidance.Revised Procedures 3/4-OP-074,informed Personnel of Event & Performed Walkdown of CR
ML17354B0001998-03-18018 March 1998 Florida Power & Light Topical Quality Asurance Rept, Dtd June 1998 05000250/LER-1998-001-02, :on 980216,manual Reactor Trip Occurred Due to Loss of Turbine Control Oil Pressure W/Steam Leak in Auxiliary Feedwater Steam Supply Piping.Auxiliary Governor Maint Instructions Will Be Revised1998-03-18018 March 1998
- on 980216,manual Reactor Trip Occurred Due to Loss of Turbine Control Oil Pressure W/Steam Leak in Auxiliary Feedwater Steam Supply Piping.Auxiliary Governor Maint Instructions Will Be Revised
1999-09-30
[Table view] |
text
ACCESSION NBR F*C IL: 50-250 AUTH. NAME HART> R. D.
WOODYI C. O.
RECIP. NAME REGULA Y INFORMATION D ISTR IBUTI "YSTEM
( R IDS )
E 8802170385 DOC. DATE: 88/02/12 NOTARIZED:
NO DOCK,ET ¹ Turkey Point Plant1 Unit 31 Florida PoUjer and Light C
05000250 AUTHOR AFFILIATION Florida PoUJer 5 Light Co.
Florida Poojer 5 Light Co.
RECIPIENT AFFILIATION
SUBJECT:
LER 88-001-00: on 880113. unit experienced turbine runback due to dropped control rod assembly 8< manual subcritical T eactor trip occurred Nhen addi control rods dropped into core.
Caused bg personnel error. Personnel counseled.
W/880212 ltT.
DISTRIBUTION CODE:
IE22D COPIES RECEIVED: LTR i
ENCL I
SIZE:
TITLE:
- 50. 73 Licensee Event Repor t (LER) I Incident Rpt1 etc.
NOTES:
REC IP IENT ID CODE/NAME PD2-2 LA ED ISONI G COPIES LTTR ENCL 1
1 1.
RECIP IENT ID CODE/NAME PD2-2 PD COPIES LTTR ENCL 1
1 INTERNAL:
ACRS MICHFL SON AEQD/DOA AEOD/DSP/ROAB
- I'M/DCT4/DAB NRR/DEST/ADS NRR/DES./ELB NRR/DEST/MFB NRR/DEST/PSB NRR/DEST/SGB NRR/DLPG/GAB NRR/DREP/RAB NP 31 02 RES/DE/EIB RGN2 FILE 01 E'XTERNAL:
EG'.iG GROHI M H ST LOBBY WARD NRC PDR NSIC MAYS, G 5
5 1
1 1
ACRS MOELLER AEOD/DSP/NAS AEOD/DSP/TPAB DEDRO NRR/DEST/CEB NRR/DEST/ICSB NRR/DEST/MTB NRR/DEST/RSB NRR/DLPG/HFB NRR/DOEA/EAB NRR/DREP/RPB NRR/PMAS/ILRB RES TELFORDi J RES/DRPS DIR FORD BLDG HOY1 A LPDR NSIC HARRISI J 1
1 1
1 1
1 1
1 1
1 1
1
'1 1
TOTAL NUMBER OF COPIES REQUIRED:
LTTR 46 ENCL 45
\\
NRC Form 366 (9 83)
LICENSEE EVENT REPORT (LER)
U.S. NUCLEAA REGULATORY COMMISSION APPROVED OMB NO. 31604104 EXPIRES: SI31ISS FACILITYNAME III DOCKET NUMBER 12)
PA E
3 0
5 0
0 0
2 5 0
~ PF0 Turke Point Unit 3 Turbine Run ac ue o
roppe on ro o
an Subcritical Reactor Trip When Additional Control Rods Dropped Into the Core EVENT DATE IS)
LER NUMBER (6I REPOR1'DATE(7)
OTHER FACILITIES INVOLVED(Sl MONTH OAY YEAR YEAR SSOVSNTIAL N VMS 6R: <4 REVISION NVMSSR MONTH OAY YEAR A
FACILITYNAMES DOCKET NUMBFRISI 0
5 0
0 0
0 1
1 3
8 8 8 8
0 0 1
0 0
2 1
2 8 8 N/A 0
5 0
0 0
OPEAATINO MODE ISI POWER LEvEL 1
0 0 20.402(ol 20.405 (~ ) I I I (ll 20.405 I~ ) I1)(ilI 20.405( ~)III(SI) 20A06(e)(1)(lvl 20.405 (e I (1)(r) 20A05(cl 50.38(c l(1) 50.36(cl(2) 60.73(el(2)(ll 60.73(el(2) (ll) 60,73(e) (2)(ill)
LICENSEE CONTACT FOR THIS LER (12I 50.73( ~ ) (2) (Ivl 50.73( ~)(2)(vl 60.73(el(2)(rill 50.73( ~)(2)(vill)(A) 50.73(eH2)
(vill)(BI 60.73( ~ )(2)(xI 0 THE REOUIREMENTS OF 10 CFR (): TCnrck onr or more ot tnr IoiroWinpl )11)
THIS REPORT IS SUBMITTED PURSUANT T 73.71(II) 73.71(cl OTHER ISprciiy In AOstrrct Oriow rnd In Trit, NRC Form 366AI NAME Randall D. Hart, Licensing Engineer TELEPHONE NUMBER AREA CODE 305 24 6 -
6 559 COMPLETE ONE I.INE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPORT 113) n'v
CAUSE
SYSTEM COMPONENT MANUFAC.
TUAER REPORTABLE TO NPRDS
CAUSE
SYSTEM COMPONENT MANUFAC TURER EPORTABL'E TO NPADS A A C
ON W 12 0
Y y
~ 'SsP~Nmngg<<
i. 2 cyyPPg<. rc 'sslp.y.
SUPPLEMENTAL REPORT EXPECTED (14)
YES (IIyes, compirte EXPECTED SUBMISSION DATE)
NO ABSTAACT I(.imit to )400 sprees, I.e., rpproximeteiy hftrrn sinrir specs typrrm'INn since) 118)
EXPECTED SUBMISSION DATE (15)
MONTH OAY YEAR On January 13, 1988, while at 100% power, Unit 3 experienced a turbine runback due to a dropped control rod assembly.
The operators commenced operating procedure (OP) 1604.1, Full Length RCC Periodic Exercise.
Step 8.4.1 was initiated to step shutdown bank A control rods, when rod control cluster (RCC) N-9 dropped into the core.
This energized the rod bottom bistable for N-9 initiating a rod position indication (RPI) turbine runback to approximately 70% power.
Off normal operating procedures were consulted to stabilize reactor power.
An attempt was made to retrieve the RCC which was unsuccessful.
The unit was shutdown to facilitate repairs.
During the shutdown sequence two more'CCs dropped and a manual reactor trip was initiated.
The unit was stabilized in mode 3.
An investigation into the root cause of the first dropped control rod determined that a pin on the connector for the movable gripper coil on the reactor head had been pushed out of engagement.
Therefore when the RCC was moved, the movable gripper coil did not engage and the RCC dropped into the core.
The other two dropped RCCs were due to personnel error in that a technician removed the power fuses to N-9 and did not identify that the power fuse to the movable gripper coil was common to two other RCCs.
The connector pins on the RCCs were inspected and engaged as necessary.
The appropriate personnel were counseled on this event.
NAC Form 366 (9 831 8802170385 880212 PDR ADDCK 05000250 8
PDR
~p I
NRC Form 388A, (94)3)
LICENSEE NT REPORT ILER) TEXT CONTINU N
U.S. NUCLEAR REGULATORY COMMISSION APPROVEO OMB NO. 3150M)04 EXPIRES: 8/31/88 FACILITYNAME (1)
OOCKET NUMBER (2)
LER NUMBER (8)
YEAR
.'+8 SEQUENTIAL Po)r NN NUMSEII REVISION NUMS E II PAGE (3)
Turke Point Unit 3 TEXT //P/Roro 4/rooo ir /<<9<<SIN/, Iroo ~ //Ro/ro////IC Forrrr 3/3/AB) (IT) 0 5
0 0
0 0
1 0 00'2 OF EVENT:
On January 13, 1988, while at 100% power, Unit 3 experienced a turbine runback due to a dropped control rod assembly (EIIS:AA).
At 0407 on January 13,
- 1988, the operators commenced operating procedure (OP) 1604.1, Full Length RCC-Periodic Exercise.
Step 8.4.1 was initiated to step shutdown bank A control
- rods, when rod control cluster (RCC) N-9 dropped into the core.
This energized the rod bottom bistable for N-9 initiating a rod position indication (RPI) turbine runback to approximately 70% power.
Off normal operating procedure (ONOP) 3-0NOP-089, Turbine Runback, was consulted to stabilize reactor power.
The Reactor Engineering Department was contacted for guidance and the recommendation was that if retrieval of the RCC was unsuccessful, reduce power to less than 50%.
At 0449, 3-0NOP-028, Reactor Control System Malfunction, was used in attempt to realign RCC N-9 with shutdown bank A.
This was unsuccessful and N-9 was declared inoperable.
At 0504 a unit load reduction to less than 50% reactor power was commenced.
An investigation by the Instrumentation and Control Department (I&C) determined that N-9 had an open circuit in the movable coil circuit.
At this time plant management decided to shutdown unit 3 to facilitate investigations.
The load reduction began at 0635 and the unit was taken off the line at 0737.
Further trouble shooting by I&C resulted in plant management deciding to shutdown the unit to cold shutdown (mode
- 5) to facilitate repairs.
At 1318, the shutdown of the unit was continued.
At 1319 with the D control rod bank at 100 steps, RCC M-10 (C control rod bank) dropped into the core.
This point corresponds to the 100 step overlap between the D and C control rod banks.
3-ONOP-028 was consulted for guidance and the reactor shutdown was continued.
At 1323, with the B control rod bank at 100 steps, RCC L-9 (A control rod bank) dropped into the core.
This point also corresponds to the 100 step overlap between control rod banks B and A.
At this point the operator manually tripped the reactor as required by 3-ONOP-028 due to the third RCC dropping into the core.
The unit was subsequently stabilized in mode 3 (hot standby).
CAUSE
OF EVENT:
An investigation into the root cause of the first dropped control rod determined that a pin on the connector for the movable gripper coil on the reactor head had been pushed partially out of engagement.
After time this pin became completely disengaged with the connector.
Therefore, when the operator attempted to move the RCC during the performance of OP 1604.8, the stationary coils disengaged from N-9, however, the movable coil did not engage on N-9 due to the pin in the connector not being engaged.
This resulted in the dropped RCC N-9.
The root cause for the partially engaged connector pin is still under investigation with the vendor.
During the shutdown, the connectors for the other RCCs were inspected for partially engaged connector pins and any discrepancies were corrected.
NRC FORM 3OSA (94)3)
<<U.S.GPO,1988 0 824 538/455
NRC Form 3EEA i (94)3)
LICENSEE NT REPORT (LER) TEXT CONTINU N
U.S. NUCLEAR REOULATORY COMMISSION APPROVED 0MB NO. 3150-0104 EXPIRES: 8/31/88 fACILITYNAME Ill DOCKET NUMBER 12)
VEAR LER NUMBER 16)
SEOVENTIAL NVMSER gi's REVISION NVMSEII PAOE 13)
TIXT///rrfrr>><<Ec>> /f EEr/rorL r>>o
//Rl>>o>>/ HRC %%drm 3/EE49/117) 0 5
0 0
0 1
OF The root cause for the other two dropped RCCs was personnel error.
When RCC N-9 was taken out of service the power fuses to the stationary, lift and movable coils were pulled.
The technician removing the fuses used an uncontrolled label located on the power supply cabinet to guide his efforts and did not use controlled documents to verify that he was not affecting any other components when he removed the fuses.
The movable coils for RCCs N-9, M-10, and L-9 share a
common neutral fuse.
Therefore, when the power fuses for N-9 were
- removed, the power to the movable coil for M-10 and L-9 was lost.
So when the RCC bank overlap initiated RCC movement, the movable coils for M-10 and L-9 did not energize and the RCCs dropped into the core.
ANALYSIS OP EVENT:
Upon initiation of the RPI rod bottom signal, a turbine runback was automatically initiated as designed.
Reactor coolant system (RCS) and secondary system parameters responded as expected for this type of event.
At the time of the reactor trip, Unit 3 was in mode 3 and in the process of inserting the control rod and shutdown banks into the core.
When the manual reactor trip signal was generated, the reactor trip breakers opened and shutdown and control rod banks inserted into the core as designed.
A post trip review was performed to assess the proper operation of safety-related equipment.
The post trip review established that the transient behavior of pertinent plant parameters for the reactor coolant system and steam generators responded as expected for a transient of this kind.
Based on the above, the health and safety of the public were not affected.
CORRECTIVE ACTIONS
1)
The connector pins for RCC N-9 were inspected and engaged properly.
The rest of the RCCs for Unit 3 were inspected for partially engaged connector pins.
Several partially engaged pins were found and corrected.
2)
The reason for the partially engaged pins is still under investigation.
Upon completion of this investigation, appropriate corrective actions will be taken.
3)
The I&C shop personnel have been counseled on the.cause of the multiple RCC drops and how to prevent future occurrences 4)
Trouble shooting procedures will be clarified to ensure that proper drawing and/or prints are consulted prior to fuse removal.
In this event a
noncontrolled label had been used to identify the fuses.
This label will be replaced.
NRC fORM SESA (94)3)
- U.S.GPO;1986 0 62 ~ 538/455~
(94)3)
LICENSEE NT REPORT ILER) TEXT CONTINU N
U.S. NUCLEAR REGULATORY COMMISSION APPROVED OMS ND. 3)50W104 EXPIRES; 8/31/68 FACILITYNAME (ll DOCKET NUMBER (2)
YEAR LER NUMBER (6) nW~'EOVENTIAL NO/
NVMSER Irido REVISION
~ '.o/ NVMEEII PAGE (3) mCT
/~RKFo EPSOF
/4~ ~~//RC r 36544)(IT) 0 5
0 0
0 OF 5)
Upon approval of the post trip review and completion of required maintenance-activities, unit 3 will be returned to service.
6)
This event will be reviewed by the Training Department to determine if additional training is warranted.
ADDITIONALDETAILS:
The control rod system is supplied by Westinghouse.
Similar Occurrences:
LERs 251-85-021 and 251-86-002 reported events where a
turbine runback occurred due to a dropped control rod.
However, the root cause for those runbacks was different from this event.
NRC FOAM 366A 194)3) o U.S.GPO:1986 0 624 538/455
P. 0 14000, JUNO BEACH, FL 33408.0420 FfBRUARY 1 2 1988 L-88-67 10 CFR 50-73 U. S. Nuclear Regulatory Commission Attn:
Document Control Desk Washington, D.
C.
20555 Gentlemen:
Re:
Turkey Point Unit 3 Docket No. 50-250 Reportable Event:
88-01 Date of Event:
January 13, 1988 Turbine Runback Due to Dropped Control Rod and Subsequent Manual Subcritical Reactor Trip When The Additional Control Rods Dro ed Into the Core The attached Licensee Event Report (LER) is being submitted pursuant to the requirements of 10 CFR 50.73 to provide notification of the subject event.
Very truly yours, G4d g C.
O.
Execut ody e Vice President COW/SDF/gp Attachment cc:
Dr. J.
Nelson Grace, Regional Administrator, Region II, USNRC Senior Resident Inspector, USNRC, Turkey Point Plant SDF/012. LER
~8 i I an FPL Group company
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05000250/LER-1988-001, :on 880113,unit Experienced Turbine Runback Due to Dropped Control Rod Assembly & Manual Subcritical Reactor Trip Occurred When Addl Control Rods Dropped Into Core. Caused by Personnel Error.Personnel Counseled |
- on 880113,unit Experienced Turbine Runback Due to Dropped Control Rod Assembly & Manual Subcritical Reactor Trip Occurred When Addl Control Rods Dropped Into Core. Caused by Personnel Error.Personnel Counseled
| | 05000251/LER-1988-001-01, :on 880129,operability Requirements of Tech Spec 3.5.1 for Steam Generator lo-lo Level Reactor Could Not Be Met.Caused by Procedural Error.Setpoints of Affected Channels Rechecked,Calibr & Procedure Revised |
- on 880129,operability Requirements of Tech Spec 3.5.1 for Steam Generator lo-lo Level Reactor Could Not Be Met.Caused by Procedural Error.Setpoints of Affected Channels Rechecked,Calibr & Procedure Revised
| 10 CFR 50.73(a)(2) | 05000251/LER-1988-002-01, :on 880202,containment & Control Room Ventilation Isolation Occurred.Caused by Personnel Error While Performing Mod to Remove Remote Alarm Function.Planner & Technician Involved Counselled |
- on 880202,containment & Control Room Ventilation Isolation Occurred.Caused by Personnel Error While Performing Mod to Remove Remote Alarm Function.Planner & Technician Involved Counselled
| 10 CFR 50.73(e)(2) | 05000250/LER-1988-002, :on 880115,RCS Pressure Decreased to 625 Psig & Accumulators Started to Inject.Caused by Defective Controller for Valve PCV-3-455B.Controller Replaced |
- on 880115,RCS Pressure Decreased to 625 Psig & Accumulators Started to Inject.Caused by Defective Controller for Valve PCV-3-455B.Controller Replaced
| 10 CFR 50.73(e)(2)(v) | 05000250/LER-1988-003, :on 880308,containment Ventilation & Control Room Ventilation Isolation Occurred.Caused by Minor Electrical Transient Upon Failure of One Light Filament. Failed Dual Filament Bulb Replaced |
- on 880308,containment Ventilation & Control Room Ventilation Isolation Occurred.Caused by Minor Electrical Transient Upon Failure of One Light Filament. Failed Dual Filament Bulb Replaced
| 10 CFR 50.73(e)(2) | 05000251/LER-1988-003-01, :on 880207,shutdown of Unit from 100% Power Commenced Due to Exceeding Requirements of Tech Spec for Having Battery Charger 4S Out of Svc.Caused by Failure of Snubber Capacitor.Capacitor Replaced |
- on 880207,shutdown of Unit from 100% Power Commenced Due to Exceeding Requirements of Tech Spec for Having Battery Charger 4S Out of Svc.Caused by Failure of Snubber Capacitor.Capacitor Replaced
| 10 CFR 50.73(c)(2) | 05000250/LER-1988-004, :on 880318,auxiliary Feedwater Pumps Actuated Due to Drop in Steam Generator Level.Caused by Reactor Control Operator Failure to Monitor Steam Generator Level. Operator Counseled Re Awareness of Actions |
- on 880318,auxiliary Feedwater Pumps Actuated Due to Drop in Steam Generator Level.Caused by Reactor Control Operator Failure to Monitor Steam Generator Level. Operator Counseled Re Awareness of Actions
| 10 CFR 50.73(e)(2) | 05000251/LER-1988-004-02, :on 880408,Tech Spec Table 3.5-2 Requirements Exceeded.Caused by Failure of Relays 327TX/4A2 & 327TX/4A2 in Undervoltage Protection Scheme for 4A 480 Volt Load Ctr. Relays Replaced & Tested |
- on 880408,Tech Spec Table 3.5-2 Requirements Exceeded.Caused by Failure of Relays 327TX/4A2 & 327TX/4A2 in Undervoltage Protection Scheme for 4A 480 Volt Load Ctr. Relays Replaced & Tested
| | 05000251/LER-1988-004-03, :on 880408,Tech Spec 3.5-2,Item 3.2.b Exceeded. Caused by Failure of Relays in Undervoltage Protection Scheme.Relays Replaced & Satisfactorily Tested Before Unit Shutdown Commenced |
- on 880408,Tech Spec 3.5-2,Item 3.2.b Exceeded. Caused by Failure of Relays in Undervoltage Protection Scheme.Relays Replaced & Satisfactorily Tested Before Unit Shutdown Commenced
| 10 CFR 50.73(e)(2)(iv) | 05000251/LER-1988-004, Forwards Corrected LER 88-004,correcting Event Date in Block 5 of Rept Form as Submitted W/Util | Forwards Corrected LER 88-004,correcting Event Date in Block 5 of Rept Form as Submitted W/Util | | 05000251/LER-1988-005-01, :on 880425,calibr of Nuclear Instrumentation Sys Power Range Detectors Performed Late.Caused by Personnel Error.Digital Data Processing Sys Repaired & Group Responsible for Performance Discussed Event |
- on 880425,calibr of Nuclear Instrumentation Sys Power Range Detectors Performed Late.Caused by Personnel Error.Digital Data Processing Sys Repaired & Group Responsible for Performance Discussed Event
| | 05000250/LER-1988-005, :on 880415,loss of Flowpath from Boric Acid Storage Tanks to RCS Occurred.Caused by Loose Screw in Motor/Pump Coupling.Boric Acid Transfer Pump 4A Realigned to Provide Boric Acid Flow Path to Unit 3 |
- on 880415,loss of Flowpath from Boric Acid Storage Tanks to RCS Occurred.Caused by Loose Screw in Motor/Pump Coupling.Boric Acid Transfer Pump 4A Realigned to Provide Boric Acid Flow Path to Unit 3
| | 05000251/LER-1988-006-01, :on 880716,containment Ventilation & Control Room Ventilation Sys Isolation Occurred.Caused by Very Conservative Setpoint for R-11 Actuation.Unit Removed from Operation & Temporary Repair Effected |
- on 880716,containment Ventilation & Control Room Ventilation Sys Isolation Occurred.Caused by Very Conservative Setpoint for R-11 Actuation.Unit Removed from Operation & Temporary Repair Effected
| 10 CFR 50.73(e)(2) | 05000250/LER-1988-006, :on 880408,surveillance of Hydrogen & Oxygen Concentration of Inservice Gas Decay Tank Missed.Caused by Personnel Error.Surveillance Incorporated Into Chemistry Primary Daily Worksheet & Personnel Counseled |
- on 880408,surveillance of Hydrogen & Oxygen Concentration of Inservice Gas Decay Tank Missed.Caused by Personnel Error.Surveillance Incorporated Into Chemistry Primary Daily Worksheet & Personnel Counseled
| 10 CFR 50.73(e)(2) 10 CFR 50.73(e)(2)(ii) | 05000250/LER-1988-007, :on 880427,3A Intake Cooling Water (Icw) Pump out-of-svc Due to Discharge Pressure Gauge Piping Failure. Caused by Corrosion of Coupling Attaching Pressure Gauge Piping to Icw Discharge Pipe.Piping Repaired |
- on 880427,3A Intake Cooling Water (Icw) Pump out-of-svc Due to Discharge Pressure Gauge Piping Failure. Caused by Corrosion of Coupling Attaching Pressure Gauge Piping to Icw Discharge Pipe.Piping Repaired
| 10 CFR 50.73(e)(2)(vii) 10 CFR 50.73(e)(2) 10 CFR 50.73(e)(2)(ii) | 05000251/LER-1988-007-01, :on 880812,while Performing Corrective Maint, Subcritical Reactor Trip Occurred.Caused by Failure of Source Range Neutron Detector N-32.Post-trip Review Performed & Detector Replaced |
- on 880812,while Performing Corrective Maint, Subcritical Reactor Trip Occurred.Caused by Failure of Source Range Neutron Detector N-32.Post-trip Review Performed & Detector Replaced
| | 05000251/LER-1988-008-01, :on 880815,Phase a of Containment Isolation Train a Actuated.Caused by Wire Bundle Bouncing Contacts of Relay 4-SIA2.Actuation Signal Reset |
- on 880815,Phase a of Containment Isolation Train a Actuated.Caused by Wire Bundle Bouncing Contacts of Relay 4-SIA2.Actuation Signal Reset
| 10 CFR 50.73(s)(2)(i) 10 CFR 50.73(s)(2)(v) 10 CFR 50.73(s)(2) | 05000250/LER-1988-008, :on 880613,flowpath Which Could Result in Insufficient NPSH to Certain Pumps During LOCA Recirculation Identified.Procedures Revised to Maintain Valve 887 Locked in Fully Open Position |
- on 880613,flowpath Which Could Result in Insufficient NPSH to Certain Pumps During LOCA Recirculation Identified.Procedures Revised to Maintain Valve 887 Locked in Fully Open Position
| 10 CFR 50.73(e)(2) | 05000250/LER-1988-009, :on 880527,determined That Tech Spec Surveillances for Station Battery Pilot Cell Rotation Not Properly Implemented in 1987.Caused by Personnel Error & Procedure Inadequacy.Training Bulletin Issued |
- on 880527,determined That Tech Spec Surveillances for Station Battery Pilot Cell Rotation Not Properly Implemented in 1987.Caused by Personnel Error & Procedure Inadequacy.Training Bulletin Issued
| | 05000251/LER-1988-009, :on 880816,steam Generator Feedwater Pump Tripped During Coating of Condensate Polisher Vessel 4B W/ Resin for Secondary Sys Startup.Caused by Failure of Differential Pressure Switch.Switch Replaced |
- on 880816,steam Generator Feedwater Pump Tripped During Coating of Condensate Polisher Vessel 4B W/ Resin for Secondary Sys Startup.Caused by Failure of Differential Pressure Switch.Switch Replaced
| | 05000251/LER-1988-010-01, :on 880819,reactor Trip Occurred Due to lo-lo Steam Generator B Level.Caused by Cognitive Personnel Error. Reactor Control Operator Counseled Re Procedural Compliance & Attention to Details |
- on 880819,reactor Trip Occurred Due to lo-lo Steam Generator B Level.Caused by Cognitive Personnel Error. Reactor Control Operator Counseled Re Procedural Compliance & Attention to Details
| 10 CFR 50.73(e)(2) | 05000250/LER-1988-010, :on 880528,containment Ventilation & Control Room Ventilation Isolation Occurred While Containment Radiation Monitor Setpoint Being Checked.Drawer for Monitor R-11 Initiated Signals.Drawer Replaced |
- on 880528,containment Ventilation & Control Room Ventilation Isolation Occurred While Containment Radiation Monitor Setpoint Being Checked.Drawer for Monitor R-11 Initiated Signals.Drawer Replaced
| 10 CFR 50.73(s)(2) | 05000250/LER-1988-011, :on 880529,discovered That Diesel Oil Storage Tank Isolation Valve 70-003 Locked Closed.Caused by Personnel Error.Technician Disciplined & Info Bulletin Re Work Controls & Procedural Compliance Issued |
- on 880529,discovered That Diesel Oil Storage Tank Isolation Valve 70-003 Locked Closed.Caused by Personnel Error.Technician Disciplined & Info Bulletin Re Work Controls & Procedural Compliance Issued
| 10 CFR 50.73(e)(2) | 05000251/LER-1988-011-01, :on 880816,damage Occurred to Property in Excess of $2,000 Due to Spent Fuel Pool Leakage.Caused by Pump Failure Causing Vent Valve to Vibrate Open.Floor Drain Sys Cleaned.Pump & Oiler Repaired & Inspected |
- on 880816,damage Occurred to Property in Excess of $2,000 Due to Spent Fuel Pool Leakage.Caused by Pump Failure Causing Vent Valve to Vibrate Open.Floor Drain Sys Cleaned.Pump & Oiler Repaired & Inspected
| 10 CFR 50.73(a)(2)(iv), System Actuation 10 CFR 50.73(e)(2) | 05000250/LER-1988-012, :on 880614,QA Audit Caused Investigation Into Delay in Issuing Fire Protection Impairment Form for Four Penetration Seals in Switchgear Room.Caused by Inadequate Controls.Seal Surveillance Being Generated |
- on 880614,QA Audit Caused Investigation Into Delay in Issuing Fire Protection Impairment Form for Four Penetration Seals in Switchgear Room.Caused by Inadequate Controls.Seal Surveillance Being Generated
| | 05000251/LER-1988-012-01, :on 880905,control Rod K-12 Dropped from 228 Steps to 0 Step,Causing Turbine Runback to 60% Power.Cause of Drop Under Investigation.Insp of Control Rod K-12 Will Be Performed During Current Refueling Outage |
- on 880905,control Rod K-12 Dropped from 228 Steps to 0 Step,Causing Turbine Runback to 60% Power.Cause of Drop Under Investigation.Insp of Control Rod K-12 Will Be Performed During Current Refueling Outage
| 10 CFR 50.73(e)(2) 10 CFR 50.73(e)(1)(0) | 05000250/LER-1988-013, :on 880707,discovered That Monthly Channel Functional Test Surveillance Procedure Did Not Check Sys Alarm.Caused by Personnel Error.Surveillance Procedure Corrected & Personnel Counseled |
- on 880707,discovered That Monthly Channel Functional Test Surveillance Procedure Did Not Check Sys Alarm.Caused by Personnel Error.Surveillance Procedure Corrected & Personnel Counseled
| | 05000250/LER-1988-014, :on 880714,RCS Leakage Surveillance Not Performed within Required Interval Due to Personnel Error. Note Placed in Night Book Stressing Need to Meet 18-30 H Tech Specs Requirements |
- on 880714,RCS Leakage Surveillance Not Performed within Required Interval Due to Personnel Error. Note Placed in Night Book Stressing Need to Meet 18-30 H Tech Specs Requirements
| 10 CFR 50.73(e)(2) | 05000250/LER-1988-015, :on 880729,valves in Flow Path Between Hydrogen Monitors & Containment Bldg Not Verified in Proper Position. Caused by Inadequate Administrative Controls.Procedures Revised to Verify Valve Position |
- on 880729,valves in Flow Path Between Hydrogen Monitors & Containment Bldg Not Verified in Proper Position. Caused by Inadequate Administrative Controls.Procedures Revised to Verify Valve Position
| | 05000250/LER-1988-016, :on 880811,containment Spray Pump out-of-svc for Maint Exceeding Tech Specs Limits.Caused by Lack of Knowledge Re Need for break-in Period for New Bearings. Training Procedures to Be Revised |
- on 880811,containment Spray Pump out-of-svc for Maint Exceeding Tech Specs Limits.Caused by Lack of Knowledge Re Need for break-in Period for New Bearings. Training Procedures to Be Revised
| 10 CFR 50.73(e)(2) | 05000250/LER-1988-017, :on 880815,control Room Ventilation Sys Out of Svc in Excess of Tech Spec Time Limit Due to Intermittent Circuit Failure.Caused by Procedural Deficiency.Bridge Circuit Replaced & Plant Mod in Effect |
- on 880815,control Room Ventilation Sys Out of Svc in Excess of Tech Spec Time Limit Due to Intermittent Circuit Failure.Caused by Procedural Deficiency.Bridge Circuit Replaced & Plant Mod in Effect
| 10 CFR 50.73(e)(1) | 05000250/LER-1988-018-06, :on 880822,determined That Refueling Water Storage Tank Supply to ECCS Isolated from Both Trains of ECCS Sys.Caused by Procedure Inadequacy.Procedure Revised to Exclude Monthly Cycling of Tank Outlet Valves |
- on 880822,determined That Refueling Water Storage Tank Supply to ECCS Isolated from Both Trains of ECCS Sys.Caused by Procedure Inadequacy.Procedure Revised to Exclude Monthly Cycling of Tank Outlet Valves
| 10 CFR 50.73(e)(2) | 05000250/LER-1988-018, :on 880822,refueling Water Storage Tank Supply to ECCS Isolated from Both Trains of Eccs,Including RHR, Containment Spray & Hpsi.Caused by Procedure Inadequacy. Procedures Revised to Exclude Monthly Cycling |
- on 880822,refueling Water Storage Tank Supply to ECCS Isolated from Both Trains of Eccs,Including RHR, Containment Spray & Hpsi.Caused by Procedure Inadequacy. Procedures Revised to Exclude Monthly Cycling
| | 05000250/LER-1988-019, :on 880822,boric Acid Transfer Pump 3A Declared out-of-svc.Caused by Lack of Visible Water Level & Zero Nitrogen Pressure in Seal Pot & Failure of Pump Seal.Seal Replaced & Pump Returned to Svc |
- on 880822,boric Acid Transfer Pump 3A Declared out-of-svc.Caused by Lack of Visible Water Level & Zero Nitrogen Pressure in Seal Pot & Failure of Pump Seal.Seal Replaced & Pump Returned to Svc
| | 05000250/LER-1988-020, :on 880831,control Room Ventilation Sys Shifted to Recirculation Mode While Conducting Routine Test of Channel B Air Intake Radiation Monitor.Caused by Spurious Actuation Signal.Recirculation Mode Verified |
- on 880831,control Room Ventilation Sys Shifted to Recirculation Mode While Conducting Routine Test of Channel B Air Intake Radiation Monitor.Caused by Spurious Actuation Signal.Recirculation Mode Verified
| 10 CFR 50.73(s)(2) | 05000250/LER-1988-021, :on 880913,pressurizer PORV Stroke Time Exceeded Tech Spec Design Basis Value of 3.0 for Heat Input Case.Caused by Undersized Air & Nitrogen Backup Supply Line to Actuators.Procedures Revised |
- on 880913,pressurizer PORV Stroke Time Exceeded Tech Spec Design Basis Value of 3.0 for Heat Input Case.Caused by Undersized Air & Nitrogen Backup Supply Line to Actuators.Procedures Revised
| | 05000250/LER-1988-022, :on 880920,emergency Diesel Generator a Declared out-of-svc Due to High Fuel Oil Pressure.Diesel Generator B out-of-svc Since 880917.Caused by Excessive Particles in Filter.Filter Replaced |
- on 880920,emergency Diesel Generator a Declared out-of-svc Due to High Fuel Oil Pressure.Diesel Generator B out-of-svc Since 880917.Caused by Excessive Particles in Filter.Filter Replaced
| 10 CFR 50.73(a)(2)(i) 10 CFR 50.72(b)(3)(ii), Degraded or Unanalyzed Condition 10 CFR 50.73(x)(2) | 05000250/LER-1988-023, :on 880926,chemistry Technician Reported That There Was No Flow Indication to Plant Process Radiation Monitor R-19.Caused by Solids from Steam Generator Blowdown. Sample Flows to R-19 Will Be Monitored |
- on 880926,chemistry Technician Reported That There Was No Flow Indication to Plant Process Radiation Monitor R-19.Caused by Solids from Steam Generator Blowdown. Sample Flows to R-19 Will Be Monitored
| | 05000250/LER-1988-024, :on 881001,RHR Pump Declared Out Svc Due to Leakage from Pump Seal.Cause Not Identified.Seal Cooler Flushed Prior to Reassembly to Remove Foreign Matl & Installation Technique Revised |
- on 881001,RHR Pump Declared Out Svc Due to Leakage from Pump Seal.Cause Not Identified.Seal Cooler Flushed Prior to Reassembly to Remove Foreign Matl & Installation Technique Revised
| | 05000250/LER-1988-025, :on 881013,determined That Potential Interaction Existed Between Emergency Diesel Generator Pump Control Sys Which Could Have Prevented Fulfillment of Safety Function.Caused by Inadequate Design |
- on 881013,determined That Potential Interaction Existed Between Emergency Diesel Generator Pump Control Sys Which Could Have Prevented Fulfillment of Safety Function.Caused by Inadequate Design
| 10 CFR 50.73(e)(2) | 05000250/LER-1988-026, :on 881107,unit Violated FSAR Design Requirements Re Hurricane Flood Protection |
- on 881107,unit Violated FSAR Design Requirements Re Hurricane Flood Protection
| | 05000250/LER-1988-027, :on 881006,mechanic Found to Be Contaminated When Exiting Containment Bldg.Specific Cause Unidentified. Addl Temporary Controls Implemented & Area Mopped |
- on 881006,mechanic Found to Be Contaminated When Exiting Containment Bldg.Specific Cause Unidentified. Addl Temporary Controls Implemented & Area Mopped
| 10 CFR 50.73(e)(2) | 05000250/LER-1988-028, :on 881117,control Room Ventilation Sys Shifted to Recirculation Mode While Conducting Test of Channel B Air Intake Radiation Monitor RAI 6642.Caused by Maladjustment of Monitor During Calibr.Instruction Revised |
- on 881117,control Room Ventilation Sys Shifted to Recirculation Mode While Conducting Test of Channel B Air Intake Radiation Monitor RAI 6642.Caused by Maladjustment of Monitor During Calibr.Instruction Revised
| 10 CFR 50.73(e)(2) | 05000250/LER-1988-029, :on 881121,specialist Accidently short- Circuited Power Terminal Lead Which Resulted in Closure of RHR Suction Isolation Valve MOV-3-750.Caused by Personnel Error.Personnel Briefed |
- on 881121,specialist Accidently short- Circuited Power Terminal Lead Which Resulted in Closure of RHR Suction Isolation Valve MOV-3-750.Caused by Personnel Error.Personnel Briefed
| 10 CFR 50.73(e)(2) 10 CFR 50.73(e)(1) | 05000250/LER-1988-030, :on 881202,determined That Safety Injection Accumulator Level Tech Spec Limits Possibly Exceeded During Operation.Caused by Errors in Design Which Installed Transmitters.Transmitters Being Replaced |
- on 881202,determined That Safety Injection Accumulator Level Tech Spec Limits Possibly Exceeded During Operation.Caused by Errors in Design Which Installed Transmitters.Transmitters Being Replaced
| | 05000250/LER-1988-031, Has Been Canceled.Resolution of LERs Missing from Lertrk/Scss/Dcs Discussed | Has Been Canceled.Resolution of LERs Missing from Lertrk/Scss/Dcs Discussed | | 05000250/LER-1988-032, :on 881202,personnel Error Resulted in Loss of Power to Vital Instrument Bus & Isolation of Stated Ventilation Sys.Operator Counseled.Spare Inverter Relabeled as Spare & Procedures Revised |
- on 881202,personnel Error Resulted in Loss of Power to Vital Instrument Bus & Isolation of Stated Ventilation Sys.Operator Counseled.Spare Inverter Relabeled as Spare & Procedures Revised
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