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~, ACCELERATED 'DI TRJBUTION DEMONSTRATION SYSTEM REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:9006260064 DOC.DATE: 90/06/15 NOTARIZED:
NO
. FACIL:50-250 Turkey Point Plant, Unit 3, Florida Power and Light C AUTH.NAME AUTHOR AFFILIATION POWELL,D.R.
Florida Power
& Light Co.
HARRIS,K.N.
Florida Power
& Light Co.
RECIP.NAME RECIPIENT AFFILIATION DOCKET 1T 05000250
SUBJECT:
LER 90-001-01:on 900112,liqiud effluent process radiation monitor R-18 inoperable during liquid release.
W/9 DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE:
TITLE: 50.73/50.9 Licensee Event Report (LER), Incident pt, etc.
NOTES RECIPIENT ID CODE/NAME PD2-2 LA EDISON,G INTERNAL: ACNW AEOD/DSP/TPAB DEDRO NRR/DET/EMEB9H3 NRR/DLPQ/LPEB10 NRR/DREP/PRPB11 NRR/DST/SICB 7E NRR/DST/SRXB SE RES/DS IR/EIB EXTERNAL: EG&G STUART,V.A LPDR'SIC MAYS,G NUDOCS FULL TXT COPIES LTTR ENCL 1
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'ECIPIENT ID CODE/NAME PD2-2 PD AEOD/DOA AEOD/ROAB/DSP NRR/DET/ECMB 9H NRR/DLPQ/LHFB11 NRR/DOEA/OEAB11 NRR/DST/SELB SD L ST LOBBY WARD NRC PDR NSIC MURPHY,G.A COPIES LTTR ENCL 1
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1 NOTE TO ALL"RIDS" RECIPIENTS:
r PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM P 1-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED:
LTTR 34 ENCL 34 r
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PAL gUN i5 1990 L-90-218 10 CFR 50..73 U. S. Nuclear Regulatory Commission Attn:
Document Control Desk Washington, D.
C.
20555 Gentlemen:
Re:
Turkey Point Units 3 and 4
Dockets No.
50-250 and 50-251 Reportable Event:
90-001 Revision 1
Date of Event:
January 12,
- 1990, Liquid Effluent Process Radiation Monitor R-18 Inoperable Durin a Li uid Release Due to a Control Circuit Malfunction The attached Licensee Event Report is being submitted pursuant to the requirements of 10 CFR 50.73 to provide supplemental information on the subject event.
Very,truly yours,
~
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A i",(
K. N.
arris Vice resident Turkey Point Plant KNH/DRP/DWH/rat attachment cc:
Stewart E. Ebneter, Regional Administrator, Region II, USNRC Senior Resident Inspector, USNRC, Turkey Point Plant arr FPL Group cornpsng
NAC foiiil$55 (94$ l LICENSEE EVENT REPORT (LER)
U.S, HUCLEAII AEOULATOAYCOMMISSION APPAOVEO OMS NO. $1500105 EXPIRES.'/$ 1(N fACILITYNAME Ill DOCKET NUMSEA (2)
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- NAME, LICENSEE CONTACT POA THIS LER (12)
David R. Powell, Licensing Superintendent TELEPHONE HLiMSER AREA CODE 305 246-6 55 9
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No EXPECTED SU 5 MI$$ ION DATE (15I ASSTAACT ILIIstt to tc00 tenn i t eooroei etety a(tees Iihpie Ioece tpoewstres hhnt (lsl At 1043, on January 12, 1990, with Unit 3 in Mode 1 at 100 percent power and Unit 4 in Mode 4 (Hot Shutdown),
a Reactor Control Operator (RCO) noted at the end of a release that the liquid effluent Process Radiation Monitor (PRM R-18) channel had failed.
The ratemeter did not have display indication, the associated chart recorder was off scale high, no alarm conditions existed, and automatic closure of con-trol valve RCV-018 had not occurred.
A similar event occurred on December 22, 1989.
The PRM R-18 vendor believes an intermittent fail-ure of the
+ 5 volt low voltage power supply within the radiation mon-itor cabinet caused these events.
Failure of the + 5 volt power supply would affect the ability to cause automatic closure of the liquid efflu-ent release path control valve upon reaching the predetermined alarm setpoint.
Cognitive error by licensed utility personnel contributed to these events.
Failure to frequently monitor the PRM R-18 channel during a release is not in accordance with Operating Procedure OP 5163.2; how-
- ever, FPL believes that the PRM R-18 channel alarm setpoint was not reached during the releases.
A review of Technical Specification Table 3.9-2, Item 1.a concluded that both events are reportable.
The low voltage power supply, processor card, timer card, and limit switch card were replaced.
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At 1043, on January 12, 1990, with Unit 3 in Mode 1
(Power Operation) at 100 per-cent power and Unit 4 in Mode 4 (Hot Shutdown:
average reactor coolant tempera-ture between 200 degrees F and 350 degrees F),
a release of the B Monitor Tank to the environment was completed.
Upon termination, a Reactor Control Operator (RCO) noticed the following: the liquid effluent Process Radiation Monitor (PRM R-18)
(EIIS:IL, Component:MON) channel did not have ratemeter display indication, the associated chart recorder was off scale high, no alarm conditions existed and automatic closure of liquid effluent release path control valve RCV-018 had not occurred.
A review of the PRM R-18 channel r'atemeter signal output to the chart recorder indicated that display functions failed at approximately 0957.
The PRM R-18 channel was demonstrated to be operable prior to initiation of the release at 0905, as required by Operating Procedui e OP 5163.2, "Waste Disposal System-Controlled Liquid Release to the Circulating Water System."
At 1433, on January 12,
- 1990, the NRC was notified of the above.event pursuant to 10CFR50.72(b)(2)(iii)(C).
The PRM R-18 channel continuously monitors liquid effluent releases from Turkey Point Units 3 and 4.
Automatic valve closure is initiated by this monitoring channel to stop the release after exceeding a predetermined alarm setpoint or upon loss of power.
Technical Specification (TS) Table 3.9-2, Item l.a, requires the liquid radwaste effluent line gross radioactivity monitor providing automatic termination of re-lease (PRM R-18) to be operable during effluent releases.
With PRM R'-18 inoper-able, liquid effluent releases may continue provided that, prior to initiating a release:
1.
At least two independent samples are analyzed and; 2.
At least two technically qualified members of the Facility Staff inde-pendently verify the release rate calculations and discharge valving (one performs, one verifies);
Otherwise, suspend release of radioactive effluents via this pathway.
An earlier failure of the PRM R-18 channel was noticed at 1350, on December 22, 1989, during release of the A Waste Monitor Tank.
The symptoms noticed at the end of this earlier release were identical to those noticed during the January 12, 1990 event.
The PRM R-18 channel had been demonstrated to be operable pr ior to initiation of the release at 1304, as required by Operating Procedure OP 5163.2.
A review of the PRM R-18 channel ratemeter signal output to the chart recorder indicates that the display functions failed at approximately 1305.
Ver-ification that the release'had been terminated was interpreted as meeting the conditions of TS 3.9-2, Item 1.a.
The ribbon cable connector to the PRM R-18 channel ratemeter was cleaned and tightened.
No further investigation into the cause of the noticed symptoms was performed.
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CAUSE
OP THE EVENT The only fault identified during troubleshooting the PRM R-18 channel failure was a slight loss of regulation on the -
15 volt low voltage power supply.
A total loss of the -
15 volt low voltage power supply would produce alarms on the monitor; therefore, this condition was not responsible for the PRM R-18 channel failure.
The low voltage power supply was removed and discarded.
A new low voltage power supply was installed.
Additional troubleshooting was performed on the Central Processing Unit (CPU) and the watchdogtimer, which re-programs the CPU in the event the CPU locks-up.
The PRM R-18 channel failure could not be duplicated.
The three removable cards that compr ise the radiation monitor channel logic and contr ol circuitry were replaced.
The removable cards (processor, timer/alarm and limit switch) were sent to the vendor (Nuclear Research Corp.) for further analysis.
The vendor was unable to produce a failure in the three removable cards that
.comprise the radiation monitor channel logic and control circuitry.
However,-
the vendor did duplicate the symptoms of the failure experienced in the PRM R-18 channel by removing the + 5 volt low voltage power supply to the cards.
The vendor believes that an intermittent failure of the
+ 5 volt low voltage power supply was the cause for the PRM'R-18 channel failure.
Because this low voltage power supply was discarded after being replaced during earlier troubleshooting, further analysis of the PRM R-18 channel failure to the component level can not be perfor med.
Cognitive errors by licensed utility personnel contributed to these events.
Operating Procedure OP 5163.2, Step 4.2, Precautions and Limits, requires the PRM R-18 channel to be frequently observed during a release to be assured that countrate is not approaching the setpoint stated on the liquid release permit.
Section 8.0, Instructions, contains requirements for the Auxiliary Building operator to request the RCO to periodically monitor the PRM R-18 channel and notify him if the indication approaches the alarm setpoint.
An unmonitored release condition lasted for approximately 46 minutes on January 12, 1990 and for approximately 45 minutes on December 22, 1989.
In both events, the failed PRM R-18 channel condition was not discovered until the end of the release.
ANALISIS OP THE EVENT A sample of the remaining tank contents determined that radioactivity concentra-tions were lower than at initiation of the release for both events.
Because of
.this, FPL believes the PRM R-18 channel alarm setpoints were not reached.
Addi-tionally, the radioactivity concentrations released were within the limiting com-bined Maximum Permissible Concentrations (MPC) allowed by 10CFR20, Appendix B, at the release point when averaged over a time period of one hour.
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CORRECTIVE ACTIONS
1.
An On The Spot Change (OTSC) has been generated against Operating Proce-dure OP 5163.2, "Waste Disposal System Controlled Liquid Release to the Circulating Water System,"
which requires the RCO to record PRM R-18 chan-nel readings on the Liquid Release Permit every 15 minutes during a liquid effluent release.
2.
An On The Spot Change (OTSC) has been generated against Nuclear Chemistry procedure NC-44, "Preparation of a Liquid Release Permit," which revises the Liquid Release Permit form to require the recording of PRM R-18 chan-nel readings at 15 minute intervals.
3.
The low voltage power supply, processor
- card, timer card and limit switch card were replaced.
The PRM R-18 channel tested satisfactorily and was re-turned to service.
4.
The replaced cards were returned to the vendor (Nuclear Research Corp.) for evaluation.
The vendor was unable to produce a failure in the replaced cards.
However, the vendor did duplicate the symptoms of the failure ex-perienced in the PRM R-18 channel by removing the
+ 5 volt low voltage power supply to the cards.
ADDITIONAL INFORMATION
The PRM R-18 microprocessor based ratemeter/controller is a Model DRM-200 RemRad monitoring system manufactured by Nuclear Research Corporation (NRC) Industries.
No similar Licensee Event Reports have been submitted for Turkey Point Unit 3 or 4 ~
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| 05000250/LER-1990-001, :on 891222 & 900112,liquid Effluent Radiation Monitor R-18 Failed & Ratemeter Did Not Have Display Indication.Caused by Control Circuit Malfunction.Low Voltage Power Supply Processor & Timer Cards Replaced |
- on 891222 & 900112,liquid Effluent Radiation Monitor R-18 Failed & Ratemeter Did Not Have Display Indication.Caused by Control Circuit Malfunction.Low Voltage Power Supply Processor & Timer Cards Replaced
| | | 05000251/LER-1990-001-03, :on 900228,isolation Valve for Intake Cooling Water (Icw) Pump 4C Discharge Line Pressure Indicator Was Not Correct Valve Type.Caused by Personnel Error.Valve Replaced W/Correct Valve Type |
- on 900228,isolation Valve for Intake Cooling Water (Icw) Pump 4C Discharge Line Pressure Indicator Was Not Correct Valve Type.Caused by Personnel Error.Valve Replaced W/Correct Valve Type
| | | 05000251/LER-1990-002-02, :on 900228,post-accident Containment Vent Found Inoperable for 13 Days,Contrary to Tech Spec Limit. Caused by Personnel Error.Cautions Added to Local Leak Rate Test Procedure |
- on 900228,post-accident Containment Vent Found Inoperable for 13 Days,Contrary to Tech Spec Limit. Caused by Personnel Error.Cautions Added to Local Leak Rate Test Procedure
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000251/LER-1990-002, :on 900228,Unit 4 post-accident Containment Vent Remained Inoperable More than 7 Days.Caused by Personnel Error.Operating Procedure 13404.1, Local Leak Rate Tests, Revised |
- on 900228,Unit 4 post-accident Containment Vent Remained Inoperable More than 7 Days.Caused by Personnel Error.Operating Procedure 13404.1, Local Leak Rate Tests, Revised
| | | 05000250/LER-1990-002, :on 900118,discovered That post-maint Testing Not Performed on Phase a Containment Isolation Valve CV-3-6275B After Adjusting Valve Stem Packing.Caused by Personnel Error.Personnel Counseled |
- on 900118,discovered That post-maint Testing Not Performed on Phase a Containment Isolation Valve CV-3-6275B After Adjusting Valve Stem Packing.Caused by Personnel Error.Personnel Counseled
| | | 05000250/LER-1990-003-01, :on 900220,mechanical Seal Failure Occurred on 3B Spent Fuel Pool Cooling Pump.Caused by Fatigue Failure Due to Formation of Notch Which Acted as Stress Intensifier. Spent Fuel Pump 3A Aligned as Primary Pump |
- on 900220,mechanical Seal Failure Occurred on 3B Spent Fuel Pool Cooling Pump.Caused by Fatigue Failure Due to Formation of Notch Which Acted as Stress Intensifier. Spent Fuel Pump 3A Aligned as Primary Pump
| | | 05000251/LER-1990-003-02, :on 900409,reactor Protection Sys Actuation Occurred Due to Failure of Reactor Coolant Pump Underfrequency Relay Power Supply Capacitor.Caused by Open Supply Breakers.Relay Replaced |
- on 900409,reactor Protection Sys Actuation Occurred Due to Failure of Reactor Coolant Pump Underfrequency Relay Power Supply Capacitor.Caused by Open Supply Breakers.Relay Replaced
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000250/LER-1990-003, :on 900220,determined That Spent Fuel Pool 3B Shaft Failure Resulted in Damage to Pump Mechanical Seal & Release of Borated Contaminated Water.Procedure O-PMM-061.1 Revised |
- on 900220,determined That Spent Fuel Pool 3B Shaft Failure Resulted in Damage to Pump Mechanical Seal & Release of Borated Contaminated Water.Procedure O-PMM-061.1 Revised
| | | 05000251/LER-1990-004, :on 900526,reactor Manually Tripped During Restoration Phase of Turbine Valve Test.Caused by Personnel Error.Procedures 3-OSP-089 & 4-OSP-089 Revised to Clarify Intent of Step 7.2.59 |
- on 900526,reactor Manually Tripped During Restoration Phase of Turbine Valve Test.Caused by Personnel Error.Procedures 3-OSP-089 & 4-OSP-089 Revised to Clarify Intent of Step 7.2.59
| | | 05000250/LER-1990-004, :on 900306,surveillance Test of Emergency Diesel Generator Not Completed.Caused by Misinterpretation by Sys Engineer of Safety Evaluation for 4,160 Volt Bus Outage.Personnel Reinstructed |
- on 900306,surveillance Test of Emergency Diesel Generator Not Completed.Caused by Misinterpretation by Sys Engineer of Safety Evaluation for 4,160 Volt Bus Outage.Personnel Reinstructed
| 10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications | | 05000251/LER-1990-005-02, :on 900605,intake Cooling Water Flow Rate to Component Cooling Water HXs Verified to Be Below Caution Level.Caused by Inadequate Administrative Controls.Special Instructions Initiated for supervisor-nuclear |
- on 900605,intake Cooling Water Flow Rate to Component Cooling Water HXs Verified to Be Below Caution Level.Caused by Inadequate Administrative Controls.Special Instructions Initiated for supervisor-nuclear
| | | 05000250/LER-1990-005, :on 900316,health Physics Shift Supervisor Found to Be Contaminated While Exiting Containment Bldg. Cause Not Yet Identified.Frequency of Hot Particle Surveys for Check Valve Tent Increased |
- on 900316,health Physics Shift Supervisor Found to Be Contaminated While Exiting Containment Bldg. Cause Not Yet Identified.Frequency of Hot Particle Surveys for Check Valve Tent Increased
| | | 05000250/LER-1990-006, :on 900406,control Room Ventilation Sys for Common Control Room of Units Tripped While Performing Procedure TP-584.Caused by Personnel Error.Individual Counseled |
- on 900406,control Room Ventilation Sys for Common Control Room of Units Tripped While Performing Procedure TP-584.Caused by Personnel Error.Individual Counseled
| 10 CFR 50.73(a)(2)(iv), System Actuation | | 05000251/LER-1990-006-02, :on 900705,automatic Start of Component Cooling Water Pump 4B Occurred Due to Low Pump Discharge Header Pressure.Caused by Personnel Error.Responsible Individual Required to Review Procedure |
- on 900705,automatic Start of Component Cooling Water Pump 4B Occurred Due to Low Pump Discharge Header Pressure.Caused by Personnel Error.Responsible Individual Required to Review Procedure
| 10 CFR 50.73(a)(2) 10 CFR 50.73(e)(2) | | 05000250/LER-1990-007, :on 900408,CCW Pump 3B Automatically Started Due to Low Pump Discharge Header Pressure.Caused by Inadequate Procedural Controls in Operating Surveillance Procedure 3-OSP-030.7.Procedures Changed |
- on 900408,CCW Pump 3B Automatically Started Due to Low Pump Discharge Header Pressure.Caused by Inadequate Procedural Controls in Operating Surveillance Procedure 3-OSP-030.7.Procedures Changed
| 10 CFR 50.73(a)(2) | | 05000251/LER-1990-007-02, :on 900726,component Cooling Water Pump 4A Automatically Started.Caused by Error Made by Nonlicensed Personnel.Pressure Controller PC-4-611 Recalibrated |
- on 900726,component Cooling Water Pump 4A Automatically Started.Caused by Error Made by Nonlicensed Personnel.Pressure Controller PC-4-611 Recalibrated
| | | 05000250/LER-1990-008, :on 900415,Train B Safeguards Actuation Occurred During Performance of Surveillance Test Due to Component Failure |
- on 900415,Train B Safeguards Actuation Occurred During Performance of Surveillance Test Due to Component Failure
| | | 05000251/LER-1990-008-02, :on 900812,automatic Reactor Trip on low-low Steam Generator Level Occurred Due to Loss of Steam Generator 4A Feedwater Pump.Caused by Incorrect Setpoint on Agastat Trip Delay.Condensate Pump Repaired |
- on 900812,automatic Reactor Trip on low-low Steam Generator Level Occurred Due to Loss of Steam Generator 4A Feedwater Pump.Caused by Incorrect Setpoint on Agastat Trip Delay.Condensate Pump Repaired
| 10 CFR 50.73(c)(2)(vii) | | 05000250/LER-1990-009, :on 900519,breathing Air Containment Isolation Valve CV-3-6165 Found Pinned Open While in Mode 3.Caused by Inadequate Procedural Controls.Valve CV-3-6165 Placed in Correct Normal Valve Position |
- on 900519,breathing Air Containment Isolation Valve CV-3-6165 Found Pinned Open While in Mode 3.Caused by Inadequate Procedural Controls.Valve CV-3-6165 Placed in Correct Normal Valve Position
| | | 05000251/LER-1990-009-01, :on 900710,action Requirement of Tech Spec 3.3.1 Re Containment Airlock Pressure Test Not Met.Caused by Work Control Deficiencies.Computer Program Updated to Print Caution Statement on Work Orders |
- on 900710,action Requirement of Tech Spec 3.3.1 Re Containment Airlock Pressure Test Not Met.Caused by Work Control Deficiencies.Computer Program Updated to Print Caution Statement on Work Orders
| | | 05000251/LER-1990-010-01, :on 900910,Tech Spec 3.0.1 Entered Due to Train B Undervoltage Protection Circuit Being Inoperable |
- on 900910,Tech Spec 3.0.1 Entered Due to Train B Undervoltage Protection Circuit Being Inoperable
| | | 05000250/LER-1990-010, :on 900518,Mode 3 Entered W/O Having at Least One Channel of Reactor Vessel Level Monitoring Sys in Svc. Caused by Personnel Error.Heated Junction Thermocouple Breakers Closed & Procedures Revised |
- on 900518,Mode 3 Entered W/O Having at Least One Channel of Reactor Vessel Level Monitoring Sys in Svc. Caused by Personnel Error.Heated Junction Thermocouple Breakers Closed & Procedures Revised
| | | 05000250/LER-1990-011, :on 900609,hi-hi Steam Generator Water Level Turbine Trip & Subsequent Reactor Trip Occurred.Caused by Malfunction of Feedwater Regulator hand-auto Station Open Switch 3C for Valve Controller FC-3-498F |
- on 900609,hi-hi Steam Generator Water Level Turbine Trip & Subsequent Reactor Trip Occurred.Caused by Malfunction of Feedwater Regulator hand-auto Station Open Switch 3C for Valve Controller FC-3-498F
| | | 05000251/LER-1990-011-01, :on 901113,containment Spray Pumps 4A & 4B Placed Out of Svc in Violation of Tech Spec 3.4.2.a.1.Pump 4B Had No Oil in Bearing Oiler.Cause Undetermined.Bearing Oiler Refilled W/Oil |
- on 901113,containment Spray Pumps 4A & 4B Placed Out of Svc in Violation of Tech Spec 3.4.2.a.1.Pump 4B Had No Oil in Bearing Oiler.Cause Undetermined.Bearing Oiler Refilled W/Oil
| | | 05000250/LER-1990-012, :on 900613,determined That Use of Single Reset Pushbutton for Both Trains of Containment Spray Outside Design Basis of Plants.Caused by Inadequate Design.Procedure Change Requests Generated |
- on 900613,determined That Use of Single Reset Pushbutton for Both Trains of Containment Spray Outside Design Basis of Plants.Caused by Inadequate Design.Procedure Change Requests Generated
| | | 05000251/LER-1990-012-01, :on 901221,emergency Diesel Generator Acceptance Test Stopped Due to Declining Coolant Water Level.Caused by Coolant Manifold.Defective Manifold Replaced by Vendor |
- on 901221,emergency Diesel Generator Acceptance Test Stopped Due to Declining Coolant Water Level.Caused by Coolant Manifold.Defective Manifold Replaced by Vendor
| | | 05000251/LER-1990-013-01, :on 901212,failure of Alternate DC Supply Occurred.Caused by Failed 4A & 4B EDG Pilot Exciter Regulators.Edg 4B Returned to Vendor for Repair & Transistor Replaced |
- on 901212,failure of Alternate DC Supply Occurred.Caused by Failed 4A & 4B EDG Pilot Exciter Regulators.Edg 4B Returned to Vendor for Repair & Transistor Replaced
| | | 05000250/LER-1990-013, :on 900615,reactor Trip Occurred When Operator Raised Power Above 10% W/Turbine in Tripped Condition.Caused by Personnel Error.Event Reviewed W/Operations Personnel & Operator Training in Selfchecking Initiated |
- on 900615,reactor Trip Occurred When Operator Raised Power Above 10% W/Turbine in Tripped Condition.Caused by Personnel Error.Event Reviewed W/Operations Personnel & Operator Training in Selfchecking Initiated
| | | 05000251/LER-1990-014-01, :on 901107,crack Approx Three Inches Discovered in Coolant Water Flexible Hose Flange Weld.Caused by Mfg Defect.New Flexible Hose Assemblies Received & Installed on 4A & 4B EDGs |
- on 901107,crack Approx Three Inches Discovered in Coolant Water Flexible Hose Flange Weld.Caused by Mfg Defect.New Flexible Hose Assemblies Received & Installed on 4A & 4B EDGs
| | | 05000251/LER-1990-014, :on 901107,crack Discovered in Coolant Water Flexible Hose Weld.Caused by Manufacturing Defect.New Flexible Cooling Water Hoses Successfully Retested During Remaining EDG Acceptance Tests |
- on 901107,crack Discovered in Coolant Water Flexible Hose Weld.Caused by Manufacturing Defect.New Flexible Cooling Water Hoses Successfully Retested During Remaining EDG Acceptance Tests
| | | 05000250/LER-1990-014, :on 900627,plant Mgt Declared Both PORV Block Valves Inoperable.Caused by Unconservative Min Required Thrust Values Specified by Valve.Util Plans to Readjust PORV Block Valve Operator Torque Switches |
- on 900627,plant Mgt Declared Both PORV Block Valves Inoperable.Caused by Unconservative Min Required Thrust Values Specified by Valve.Util Plans to Readjust PORV Block Valve Operator Torque Switches
| 10 CFR 50.73(e)(2) | | 05000250/LER-1990-015, :on 900720,roving Fire Watch Failed to Complete Tech Spec Required Rounds.Caused by Cognitive Personnel Error.Individual Escorted from Site & Access Authorization to Site Terminated |
- on 900720,roving Fire Watch Failed to Complete Tech Spec Required Rounds.Caused by Cognitive Personnel Error.Individual Escorted from Site & Access Authorization to Site Terminated
| | | 05000250/LER-1990-016, :on 900801,Tech Spec 3.0.1 Entered to Repair Boric Acid Filter Discharge Isolation Valve 3-348.Caused by Exposure to Higher than Normal Temps.Diaphragm Replaced on Valve & Wrap of Heat Tracing Rerouted |
- on 900801,Tech Spec 3.0.1 Entered to Repair Boric Acid Filter Discharge Isolation Valve 3-348.Caused by Exposure to Higher than Normal Temps.Diaphragm Replaced on Valve & Wrap of Heat Tracing Rerouted
| | | 05000250/LER-1990-017, :on 900817,fire Protection Surveillance Missed Due to Personnel Error.Missed Surveillance Discovered During QA Insp.Procedure O-SME-016.4 Revised to Include App a Fire Dampers |
- on 900817,fire Protection Surveillance Missed Due to Personnel Error.Missed Surveillance Discovered During QA Insp.Procedure O-SME-016.4 Revised to Include App a Fire Dampers
| | | 05000250/LER-1990-018, :on 900917,unit Missed Fire Protection Surveillance on Switchgear Room Louver Sprays |
- on 900917,unit Missed Fire Protection Surveillance on Switchgear Room Louver Sprays
| 10 CFR 50.73(a)(2)(i) | | 05000250/LER-1990-019, :on 901003,alarm Received on Control Room Annunciator X-7/6 Indicating Heat Tracing Trouble.Caused by Inadequate Work Control.Boric Acid Transfer Pumps Aligned & Event Discussed W/Shift Supervisor |
- on 901003,alarm Received on Control Room Annunciator X-7/6 Indicating Heat Tracing Trouble.Caused by Inadequate Work Control.Boric Acid Transfer Pumps Aligned & Event Discussed W/Shift Supervisor
| | | 05000250/LER-1990-020, :on 901013,surveillance Interval of Tech Spec 4.8.2.1 Exceeded Due to Personnel Error.Personnel Involved Counseled & Procedure 4-OSP-201.3 Revised |
- on 901013,surveillance Interval of Tech Spec 4.8.2.1 Exceeded Due to Personnel Error.Personnel Involved Counseled & Procedure 4-OSP-201.3 Revised
| | | 05000250/LER-1990-021, :on 901018,determined That Length of Time CCW Headers Split for Movement of Heavy Loads Exceeded Appropriate Action Statement Time Limit That Should Have Been Imposed |
- on 901018,determined That Length of Time CCW Headers Split for Movement of Heavy Loads Exceeded Appropriate Action Statement Time Limit That Should Have Been Imposed
| | | 05000250/LER-1990-022, :on 901114,discovered That Tech Spec Required Fire Protection Surveillance Not Performed within Max Allowed Time Interval.Caused by Inadequate Administrative Controls.Memo Issued |
- on 901114,discovered That Tech Spec Required Fire Protection Surveillance Not Performed within Max Allowed Time Interval.Caused by Inadequate Administrative Controls.Memo Issued
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