05000250/LER-2011-001, Regarding Manual Reactor Trip Due to Secondary Sodium Concentrations Exceeding Chemistry Limits

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Regarding Manual Reactor Trip Due to Secondary Sodium Concentrations Exceeding Chemistry Limits
ML11130A097
Person / Time
Site: Turkey Point 
Issue date: 05/06/2011
From: Kiley M
Florida Power & Light Co
To:
Document Control Desk, Office of Nuclear Reactor Regulation
References
L-2011-173 LER 11-001-00
Download: ML11130A097 (4)


LER-2011-001, Regarding Manual Reactor Trip Due to Secondary Sodium Concentrations Exceeding Chemistry Limits
Event date:
Report date:
Reporting criterion: 10 CFR 50.73(a)(2)(iv)(A), System Actuation

10 CFR 50.73(a)(2)(i)

10 CFR 50.73(a)(2)(vii), Common Cause Inoperability

10 CFR 50.73(a)(2)(ii)(A), Seriously Degraded

10 CFR 50.73(a)(2)(viii)(A)

10 CFR 50.73(a)(2)(ii)(B), Unanalyzed Condition

10 CFR 50.73(a)(2)(viii)(B)

10 CFR 50.73(a)(2)(iii)

10 CFR 50.73(a)(2)(ix)(A)

10 CFR 50.73(a)(2)(x)

10 CFR 50.73(a)(2)(v)(A), Loss of Safety Function - Shutdown the Reactor

10 CFR 50.73(a)(2)(v)(B), Loss of Safety Function - Remove Residual Heat

10 CFR 50.73(a)(2)(i)(A), Completion of TS Shutdown

10 CFR 50.73(a)(2)(v), Loss of Safety Function

10 CFR 50.73(a)(2)(i)(B), Prohibited by Technical Specifications
2502011001R00 - NRC Website

text

0 FPL.

POWERING TODAY, EMPOWERING TOMORROW.

May 6, 2011 10 CFR § 50.73 L-2011-173 U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555-0001 Re:

Turkey Point Unit 3 Docket No. 50-250 Reportable Event: 2011-001-00 Date of Event: March 6, 2011 Manual Reactor Trip Due to Secondary Sodium Concentrations Exceeding Chemistry Limits The attached Licensee Event Report 05000250-2011-001-00 is being submitted pursuant to 10 CFR 50.73(a)(2)(iv)(A) due to a valid manual actuation of the reactor protection system and associated manual reactor trip. If there are any questions, please call Mr. Robert J. Tomonto at 305-246-7327.

Very truly yours, Michael Kiley Vice President Turkey Point Nuclear Plant Attachment cc: Regional Administrator, USNRC, Region II Senior Resident Inspector, USNRC, Turkey Point Nuclear Plant an FPL Group company

NRC FORM 366 U.S. NUCLEAR REGULATORY COMMISSION APPROVED BY OMB: NO. 3150-0104 EXPIRES: 10/31/2013 (10-2010)

Estimated burden per response to comply with this mandatory collection request: 80 hours9.259259e-4 days <br />0.0222 hours <br />1.322751e-4 weeks <br />3.044e-5 months <br />. Reported lessons learned are incorporated into the licensing process and fed back to industry. Send comments regarding burden estimate to the FOIA/Privacy Section (T-5 F53), U.S. Nuclear LICENSEE EVENT REPORT (LER)

Regulatory Commission, Washington, DC 20555-0001, or by internet e-mail to infocollects.resourse@nrc.gov, and to the Desk Officer, Office of Information and Regulatory Affairs, NEOB-10202, (3150-0104), Office of Management and Budget, Washington, DC 20503. If a means used to impose an information collection does not display a currently valid OMB control number, the NRC may not conduct or sponsor, and a person is not required to respond to, the information collection.

3 PAGE Turkey Point Unit 3 05000250 I

1 of. 3

4. TITLE Manual Reactor Trip Due to Secondary Sodium Concentrations Exceeding Chemistry Limits
6. LER NUMBER
7. REPORT DATE A
8. OTHER FACILITIES INVOLVED I

FACILITY NAME DOCKET NUMBER MONTH DAY HYEAR] YEAR SEQUENTIAL REV MONTH DAY YEAR FAILIYNMOKTNME NUMBER NO. I__________

iFACILITY NAM1E DOCKET NUMBER 3

6 2011 2011 001 00 5

6 2011

9. OPERATING MODE
11. THIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR§: (Check all that apply)

C] 20.2201(b)

El 20.2203(a)(3)(i)

El 50.73(a)(2)(i)(C)

El 50.73(a)(2)(vii) 1 [l 20.2201(d)

El 20.2203(a)(3)(ii)

[1 50.73(a)(2)(ii)(A)

El 50.73(a)(2)(viii)(A)

El 20.2203(a)(1)

El 20.2203(a)(4)

El 50.73(a)(2)(ii)(B)

El 50.73(a)(2)(viii)(B)

El 20.2203(a)(2)(i)

El 50.36(c)(1)(i)(A)

Ej 50.73(a)(2)(iii)

[I 50.73(a)(2)(ix)(A)

10. POWER LEVEL E] 20.2203(a)(2)(ii)

[I 50.36(c)(1)(ii)(A)

[E 50.73(a)(2)(iv)(A)

[] 50.73(a)(2)(x)

El 20.2203(a)(2)(iii)

[] 50.36(c)(2)

El 50.73(a)(2)(v)(A)

El 73.71(a)(4)

El 20.2203(a)(2)(iv).

El 50.46(a)(3)(ii)

El 50.73(a)(2)(v)(B)

[I 73.71(a)(5) 23%

El 20.2203(a)(2)(v)

[1 50.73(a)(2)(i)(A)

[3 50.73(a)(2)(v)(C)

El OTHER El 20.2203(a)(2)(vi)

[I 50.73(a)(2)(i)(B)

El 50.73(a)(2)(v)(D)

Specify in Abstract below or in

CORRECTIVE ACTIONS

Corrective actions involved plugging several tubes and applying an overcoat of Duromar after tube plugging to address leakage and repair of a tube-to-tubesheet interface and tubes of the 3AN and 3 BS water boxes.

Long term, the Unit 3 and Unit 4 condenser tube bundles will be replaced under the Extended Power Uprate Project.

ADDITIONAL INFORMATION

EIIS Codes are shown in the format [IEEE system identifier, component function identifier, second component function identifier (if appropriate)].

SIMILAR EVENTS

Turkey Point Unit 4 had a condenser tube leak, LER 2010-008-00, that resulted in a manual plant shutdown.