ML17333A577

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Insp Repts 50-315/96-06 & 50-316/96-06 on 960526-0713. Violations Noted.Major Areas Inspected:Operations, Maintenance,Engineering & Plant Support
ML17333A577
Person / Time
Site: Cook  
Issue date: 09/19/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17333A574 List:
References
50-315-96-06, 50-315-96-6, 50-316-96-06, 50-316-96-6, NUDOCS 9609270037
Download: ML17333A577 (50)


See also: IR 05000315/1996006

Text

U.S.

NUCLEAR REGULATORY COMMISSION

REGION III

Docket Nos:

License

Nos:

Report

No:

Licensee:

Facility:

Location:

Dates:

Inspectors:

50-315,

50-316

DPR-58,

DPR-74

50-315/96006;

50-316/96006

Indiana Michigan Power

Company

Donald C.

Cook Nuclear Generating

Plant

1 Cook Place

May 26

July 13,

1996

B. L. Bartlett, Senior Resident

Inspector

D. J. Hartland,

Resident

Inspector

C.

N. Orsini, Resident

Inspector

R. Lerch, Reactor Inspector, RIII

Approved by:

W. J.

Kropp, Chief

Reactor Projects

Branch

3

9609270037

960919

PDR

ADOCK 05000315

8

PDR

l

0

Executive

Summar

D. C.

Cook Units

1 and

2

NRC Inspection

Report 50-315/96006,

50-316/96006

This integrated

inspection included aspects

of licensee

operations,

maintenance,

engineering,

and plant support.

The report covers

a 6-week

period of resident

inspection;

in addition, it includes the results of

announced

inspections

and the follow-up to issues identified during an

Integrated

Performance

Assessment

documented

in inspection report 50-315/316-

96003.

0 erations

~

Operator performance

at the controls was observed to be good, with

excellent shift turnover,

good communications,

and professional

performance.

One exception

was noted in the identification of a

degraded

condition that did not receive

a timely operability evaluation

(Section 01.2).

~

The inspectors

observed

licensed operator performance

during the failure

of a controller and determined that there

was

a prompt and professional

response.

Good attention to the boards identified the event early,

resulting in additional operator

response

time (Section 04. 1).

~

Weaknesses

were identified in the timeliness of identification and the

quality of evaluations

regarding operability of plant equipment

~

~

~

~

~

~

(Sections El.l and El.2)

Maintenance

~

The inspectors

found the work performed under these activities to be

generally professional

and thorough.

One exception

was the self-

identified improperly performed replacement of a fuel rack arm on the

Unit

1

CD D/G (Section Ml.l).

~

The licensee

exhibited

a conservative

approach

by deciding to replace

a

degraded

but operable Unit 2 train A Reactor Trip Breaker

(RTB).

The

inspectors

also noted that the licensee's

planning, coordination,

and

communications

between the different departments

was very thorough

(Hl.2) .

En ineerin

0

Three examples of failure to follow procedure

were identified for not

performing

an operability evaluation of degraded

and potentially non-

conforming conditions in a timely manner

( Sections

El. l.b. 1 and E1.2).

The inspectors

review of the licensee's

operability evaluations

determined that they were generally

weak and

some were lacking in detail

in

a number of areas

( Section El. l.b.2).

The inspectors identified one example of a licensee corrective action

program that

had

been initiated prior to

GL 91-18 whose operability

determination

process

had not been modified after

GL 91-18 (the Large

Bore Piping Reconstitution

Program)

and this appeared

to affect the

evaluation of degraded

pipe supports identified through other mechanisms

(Section El.l.b.3) .

The inspectors

reviewed the 0.

C.

Cook Integrated

Performance

Assessment

(IPAP)

Final Analysis (inspection report 50-315/316-96003),

and

identified inspection

issues

documented

by the

IPAP team.

Various

paragraphs

and comments

were given individual item numbers.

Those item

numbers

which rose to the level of violations, unresolved

items, or

inspector follow up =items are

so identified in this report (Section

E8.2).

Re ort Details

Summar

of Plant Status

Unit

1

Unit

1 began this inspection period at

100 percent

power.

Reactor

power was

decreased

to 57 percent

Reactor Thermal

Power

(RTP) June

6,

1996 to remove the

West Main Feed

Pump from service to facilitate steam supply leak repairs.

Reactor

power was restored to 100 percent

RTP June 8,

1996.

Reactor

power

was decreased

to 93 percent

RTP June

29,

1996,

due to wain

transformer thermal limitations as

a result of increasing

ambient temperature

conditions.

Reactor

power was restored to 100 percent

RTP on June 30,

1996.

Unit 2

Unit 2 entered

and exited this reporting period in Mode

1 at

100 percent

RTP.

There were no unit shutdowns or significant power reductions.

Ol

Conduct of Operations

01. 1

General

Comments

71707

IIOI

Using Inspection

Procedure

71707, the inspectors

conducted

frequent

reviews of ongoing plant operations.

In general,

the conduct of

operations

was professional

and safety-conscious;

specific events

and

noteworthy observations

are detailed in the sections

below.

In

particular,

the inspectors

noted the good operator

performance

during

the loss of a pressure controller.

Good operator turnover for a relief

occurred

and good attention to the unit enabled

an early identification

of the instrument failure.

01.2

Control

Room Observations

a.

Ins ection

Sco

e

71707

I

The inspectors

performed routine observations

of control

room

activities, shift relief and turnover, procedural

usage

and adherence,

response

to alarms

and plant conditions,

and supervisory

command

and

control including compliance with the following procedures:

~

Operations

Department

Head Instruction

(OHI) 2000,

"Operations

Department

Guidance Policy".

b.

~

OHI - 2211,

"Haintenance of Operations

Department

Logs".

~

OHI 4011,

"Conduct of Operations

(Shift Staffing)".

~

OHI 4012,

"Conduct of Operations

(Shift Turnover)".

Observations

and Findin

s

C.

The turnovers

were conducted

in a professional

manner

and included log

reviews,

panel

walkdowns, discussions

of maintenance

and surveillance

activities in progress

or planned,

and associated

LCO time restraints,

as applicable.

Procedural

usage

and adherence

was noted to be good with

appropriate

questioning of the adequacy of the procedures

for use during

plant evolutions.

The operators

exhibited good teamwork within the shift and were observed

to communicate

when necessary

with other departments

to resolve

equipment problems.

An exception to this good communications is

discussed

further in paragraph El.l and concerned

the untimely

initiation of an operability evaluation for the leaking Unit 2 West

Essential

Service Water

(ESW) strainer discharge'check

valve.

A leaking

check valve was properly identified by an auxiliary equipment operator

and

an action request

was issued,

however,

an operability evaluation

was

not requested

of engineering.

Conclusions

Operators

acted

and reacted to various plant evolutions in a prompt

and

professional

manner.

One example

was identified where

a degraded

condition was not evaluated for operability in a timely manner.

This

issue is discussed

further in section El.l.

04

04.1

Operator

Knowledge and Performance

Prom t 0 erator

Res

onse

To A Pressure

Controller Failure

Unit 2

a 0

Ins ection

Sco

e

93702

The inspectors

assessed

the performance of the licensed operators

during

the failure of main steam

header

pressure controller 2-UPC-101.

This

controller affected the operation of the main feedwater

pumps

and prompt

operator actions

were necessary

to prevent the unnecessary

shutdown of

Unit 2.

b.

Observations

and Findin s

On June

13,

1996, Unit 2 was stable at

100 percent

RTP.

Pressure

controller 2-UPC-101 failed low without any warning.

This caused

the

secondary

control system to sense

a false low steam pressure.

As a

'esult

a separate

controller which compared

feedwater

pressure

to steam

pressure

then indicate

a high differential pressure.

This controller

I

sent

a demand signal to the two main feedwater

pumps to reduce

speed in

order to reduce the indicated high differential pressure.

As speed

was

reduced,

feedwater flow was reduce resulting in lowering steam generator

water levels.

The balance of plant reactor operator

had requested

a break from the

controls

and

a relief operator took over after

a brief turnover.

The

relief operator

observed

the drop in steam generator levels prior to the

steam generator

level deviation annunciators

actuating.

He announced

the unexpected

indications to the rest of the contt ol room operators

and

began checking his panels for possible

causes.

The unit supervisor

directed the operator to take manual control

and

then

he requested

additional assistance

from the Unit

1 control

room

personnel.

The control

room operators

then restored levels

and after

the pressure

controller was repaired,

automatic control

was re-

established.

The inspectors

entered

the control

room and began observations

of the

operating

crew approximately half-way through this event.

The

inspectors

observed:

Effective command

and control

was being effected

by shift

supervision.

None of the

SROs were at the panel

but instead the

unit supervisor

(US) was several

feet behind the

ROs providing

guidance.

The shift supervisor

(SS)

and the assistant shift

supervisor

(ASS) were at the US's desk maintaining

a broad

overview and ensuring that the reactor operators

were not

distracted.

Two of the four steam generators

did eventually

have level

deviation alarms annunciate.

As directed

by the

US, the

ROs took

manual control of the feedwater regulating valves

and restored

level.

This action was promptly and efficiently performed.

The

US and the

SS held

a crew briefing immediately following the

restoration of the level controllers in automatic.

The briefing

covered:

Mhy two of the steam generators

received level deviation

alarms

and the other

two steam generators

levels

had smaller

swings.

It was determined that

a feedwater regulating valve

was operating slowly.

An action request

was written and

subsequently

a valve's controller was tuned.

The operators

discussed

any additional actions which might

be needed,

applicable technical specifications

and the

sequence

of events.

+

A plan of repair was discussed

and each

crew member

was

asked for input concerning the event.

c.

Conclusions

The operating

crew and supervision

reacted

promptly and professionally

to the failure of main steam header

pressure controller. Effective

monitoring of control panels

and good relief turnover were also

demonstrated

by the operators.

Ml

Conduct of Naintenance

M1.1

Gener al

Comments

II. Maintenance

a.

Ins ection

Sco

e

62703

The inspectors

observed all or portions of the following work

activities:

~

1-IHP 4030.SMP. Ill

~

2-IHP 4030.SNP.120

~

2-OHP 4030.STP.018

Pressurizer

Pressure

Set

1 Surveillance

Test

Steam Generator

2

& 4 Mismatch Channel II

Surveillance Test

Steam Generator

Stop Valve Dump Valve

Surveillance Test

~

2-IHP 4030.STP.510

Train "A" Reactor Protection

System

and

Engineered

Safety Features

Reactor Trip

Breaker

and Solid State Protection

System

Automatic Trip/Actuation Logic Functional

Test.

~

JO C0036842

~

JO R0059010

~

JO R0059013

~

2-IHP. SP. C36477

0

AR A0118729

Replace Solenoid for 2-MRV-232

Replace

a fuel injection pump on the

1

CD

D/G

Replace

a fuel injection

pump

on the

1

CD

D/G

Administrative Control Procedure for

Replacement of 2-52-RTA (Unit 2, train A

reactor trip breaker).

Unit 2 West

ESW pump strainer discharge

check valve sticking open.

Observations

and Findin

s

The inspectors

found the work performed under these activities to be

generally professional

and thorough.

One exception

was the self-

identified improperly performed replacement of a fuel rack arm on the

1

CD D/G.

This resulted in the inability of the D/G to take the

100

percent load requirement.

This was self-identified during the post

maintenance

testing prior to the restoration of the

D/G to operable.

The worker error was documented

in a condition report

and the licensee's

corrective action will depend

on the results of the

CR assessment.

c.

Conclusions

Haintenance activities were generally completed thoroughly and

professionally with the proper procedures

at the work site

and in active

use.

One exception

was the improper replacement of a fuel rack arm on

the

1

CD D/G that prevented

the

D/G from reaching

100 percent load.

M1.2

Reactor Tri

Breaker

RTB

Re lacement

Unit 2

a

~

Ins ection

Sco

e

62703

and

61726

b.

On June,

10,

1996 while per forming monthly surveillance

procedure

2-IHP

4030.STP.510,

"Train 'A'PS

and

ESF Reactor Trip Breaker

and

SSPS

Automatic Trip/Actuation Logic Functional Test," the licensee

was unable

to close

RTB A from the control

room.

The licensee

determined that the

inability to close the breaker remotely did not affect breaker

operability.

The breaker

was manually closed

and remained in service

until June

22,

1996,

when the breaker

was replaced.

The inspectors

reviewed the licensee's

basis for operability and

observed

the initial troubleshooting efforts including the breaker

replacement.

Observations

and Findin

s

During performance of STP.510,

the unit was in a two hour action

statement for TS 3.3.2.1 while the reactor trip bypass

breaker

was

closed.

When

RTB A would not close,

the licensee

needed to quickly

determine the extent of the problem, the effect on breaker operability,

and whether or not repairs

could be made without exceeding

the action

statement

time limits.

The inspectors verified the licensee's

conclusion that the RTB's only

safety function was to open

on

a reactor trip signal.

The licensee

determined that the problem was limited to the closing circuit, which

was electrically isolated

from the opening circuit.

The breaker

was

manually closed

and verified to open

as required.

The breaker

was then

declared

operable

and the

LCO was exited.

The inspectors

observed

troubleshooting activities,

assessed

the licensee's

basis for

operability and did not identify any concerns.

Although

RTB A remained

operable,

the licensee

wanted to replace the

breaker

as

a conservative

measure

because

the root cause of the problem

had not been identified.

Due to the time constraints

involved with the

LCO, and the coordination of several

work groups,

(Operations,

ILC,

electrical

maintenance,

and engineering)

the licensee

wrote

a special

procedure,

2-IHP.SP.C36477,

"Administrative Control

Procedure for

Replacement

of 2-52-RTA," specifically for this evolution.

The inspectors

observed

the replacement

and associated

troubleshooting

efforts on June

22,

1996.

At this time the problem could not be

repeated,

and during testing the breaker

was successfully

closed

from

the control room.

The licensee

proceeded

with the installation

and

testing of the replacement

breaker within the time constraints of the

LCO.

Following removal, the licensee

conducted further testing

on the

malfunctioning breaker

to determine the root cause.

The inability to

close

was repeated

on an intermittent basis during bench testing.

The

problem was isolated to the closing control relay which did not fully

close

on each

demand.

The relay was scheduled

to be replaced

and the

breaker will be utilized as

a spare.

The licensee

also determined that the malfunction of the closing control

relay was not a generic concern 'as:

~

This particular breaker

had

been in service since

1982 without

exhibiting problems

and

~

No other breakers

on site had'xhibited this problem.

~

A review of industry experience with similar breakers

(Westinghouse

DB-50) did not identify similar concerns.

Conclusions

The licensee

exhibited

a conservative

approach

by deciding to replace

RTB A with it degraded

but operable.

The inspectors

also noted that the

licensee

s planning, coordination,

and communications

between the

different departments

was very thorough.

This was important due to

concerns with TS time constraints

and personnel

safety,

involved with

working on the reactor trip equipment.

III. En ineerin

El

Conduct of Engineering

El. 1

Assessment

of 0 erabilit

Evaluations

a.

Ins ection

Sco

e

37551

The inspectors

reviewed procedures,

condition reports

(CR),

and action

requests

(AR) to assess

the licensee's

capability to evaluate

degraded

and potentially non-conforming conditions.

The inspectors

intent was to

verify that the licensee

could ensure that appropriate operability

requirements

were satisfied.

b.

Observations

and Findin s

The inspectors

observed that generally the licensee

was able to properly

assess

identified conditions against license

and regulatory requirements

to ensure that the licensing basis

and operability requirements

were

maintained.

The inspectors

also determined that the licensee's

timeliness

in performing these

assessments

and the quality of these

assessments

appeared

contrary to

NRC Generic Letter (GL) 91-18,

"Information To Licensees

Regarding

Two NRC Manual Sections

On

Resolution Of Degraded

and Nonconforming Conditions

And On Operability".

In addition to the guidance contained within GL 91-18 the licensee's

procedure for documenting

and addressing

degraded

and potentially non-

conforming conditions gives requirements

for the timeliness

and quality

for performing operability evaluations

(Plant Managers Instruction

(PMI)

7030, "Corrective Action").

PHI-7030 is the licensee's

primary

mechanism

by which degraded

and potentially non-conforming conditions

are evaluated.

PHI-7030 requires the originator to initiate a condition

report

(CR) for known or suspected

adverse

conditions or events

(step

6.9.a).

PHI-7030 also defines

an adverse condition/event

as

"A non-

conformance,

deficiency, deviation, discrepancy,

or adverse

trend of

items, services

and/or administrative

systems that, if left uncorrected,

could adversely

impact safety, quality, or operability" (step 5. 1).

In

step 5.31,

PMI-7030 states,

in part,

"Prompt Operability Determination

This determination

must

be made expeditiously following identification

of a potentially degraded

condition that has the potential to impact

SSC

operability."

Unfortunately these

requirements

while strong for timeliness

were not

specific

and did not give guidance for the quality of the evaluations.

For example the requirements for timeliness

were "promptly" or

"expeditiously".

This can

be clear for major issues

but was less clear

for more subtle problems.

The licensee

had recognized this due to

previous inspector

comments

and was in the process of revising the

ambiguous

procedure to add more specific requirements

and to give

additional

guidance for the quality of the operability evaluations.

This procedure

had not been

issued at the close of this inspection.

During this assessment

period, the licensee

gave additional

temporary

10

0

guidance to plant personnel

in form of a standing

order in response

to

the issues

identified below

(Standing

Order 173,

issued July 16,

1996).

1)

Timeliness

Issues

GL 91-18 contained

recommendations

as to the timeliness of performing

prompt operability determinations

and for the performance of backup

operability determinations.

The recommended

time for performing

an

operability determination in GL 91-18 was about

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> with a few

exceptional

cases

taking longer.

In addition,

a recommended

timeliness

of the technical specification

(TS) allowed outage times

(AOT) was given

for those

components

covered

by the TS.

The following list gives

examples of where the licensee

exceeded

those

recommended

guidelines:

AR 0118729

The Unit 2 West Essential

Service Water

(ESW) discharge

check

valve was leaking-by sufficient to cause

reverse

pump rotation.

The West

ESW pump was running

and the licensee

swapped to the East

ESW pump.

During the

swap over the motor driven discharge

valves

of the West

pump were momentarily open while the East

ESW pump was

running.

During this time an auxiliary equipment operator

observed

the West

pump reverse rotation, which indicated excessive

discharge

valve leakage

and wrote

an action request

(AR).

This was identified on May 3,

1996,

however

an operability

evaluation

was not performed.

This was identified when the

inspectors

requested

a copy of the evaluation

on July 9,

1996 and

it couldn't be located.

The licensee

subsequently

performed

an

evaluation

and the evaluation determined that the

ESW system

was

operable.

After a review of the data

and discussions

with plant

personnel,

the

NRC inspectors

agreed with the licensee's

determination.

The failure to perform

a prompt operability assessment

expeditiously following the identification of a potentially

degraded

condition that had the potential to impact Structure

System

Component

(SSC) operability is

a violation of TS 6.8.1.

This failure to follow a required procedure is example

(b) of

Notice of Violation 50-315/316-96006-01.

CR 96-0022

The Unit

1

CD emergency diesel

generator

(D/G) neutral

grounding

resistor

was identified by licensee

personnel

to be incorrectly

configured (nominally 6 ohms but it was wired such that it was

actually 2.3 ohms).

The problem was identified on December

27,

1995, the

CR and

subsequent

prompt operability evaluation

were not written until

January

5,

1996.

The backup operability evaluation

was written

January

8,

1996.

The timeliness of the prompt evaluation

was

inadequate

to meet licensee

procedures.

The evaluation

which was

subsequently

performed determined that the

D/G was still operable.

The inspectors

review of the quality of the evaluation did not

identify any concerns.

The failure to perform a prompt operability assessment

expeditiously following the identification of a potentially

degraded

condition that had the potential to impact Structure

System

Component

(SSC) operability is

a violation of TS 6.8. 1.

This failure to follow a required procedure is example

(c) of

Notice of Violation 50-315/316-96006-01.

CR 96-0335

With the reactor at full power, hydraulic fluid from the Unit 2

containment jib crane spilled into the reactor cavity during

testing.

An evaluation

was performed which determined that the

fluid did not affect the operability of emergency

core cooling

system.

The spill occurred

on March 8,

1996

and the prompt operability

evaluation

was performed

on March 9,

1996.

The backup operability

evaluation

was performed

on March 13,

1996.

The licensee's

procedures

for the performance of operability evaluations

did not

clearly address

the timeliness

requirements

of the backup

operability requirements.

In the inspectors'pinion

the delay

until March 13,

1996, to perform the backup operability assessment

was excessive

but was not

a violation.

CR 96-0622

D/G Cam Follower springs

were discovered failed during testing of

the Unit 2

CD D/G.

The licensee

determined that the potential

failure was applicable to both units.

An evaluation

was performed

which determined that all four D/Gs were operable.

The event occurred

on Unit 2 on April 13,

1996.

In response

to

inspector questioning

an operability evaluation

was again

performed

and documented

on June

25,

1996.

Additional inspector

questioning resulted

in the licensee

supplementing

the evaluation

on June

26,

1996.

This issue is discussed

in more detail in

paragraph

E1.2.

The Failure to perform

a prompt operability assessment

expeditiously following the identification of a potentially

degraded

condition that

had the potential to impact Structure

12

System

Component

(SSC) operability is a violation of TS 6.8.1.

This failure to follow a required procedure is example

(a) of

Notice of Violation 50-315/316-96006-01.

2)

ualit

Of Evaluations

V

The inspectors

review of the licensee's

operability evaluations

determined that they were generally

weak and

some were lacking detail in

a number of areas.

CR 96-1097

Uni,t 2 West Essential

Service

Water

(ESW) discharge

check valve

leaking-by sufficient to cause the

pump to rotate backwards

referenced

above

as

AR 0118729.

After the inspector s brought this

issue to the licensee's

attention

CR 96-1097

was written and

a

prompt oper ability was performed.

The inspector s reviewed the prompt operability determination

contained

in the

CR and agreed with the licensee's

decision that

the

ES'W system

was still operable.

However,

one of the arguments

used

by the licensee

took credit for manual

operator action.

Specifically the evaluation stated that if the check valve stuck

open

enough to divert a large

amount of flow, the determination

took credit for the operators

manually closing the train cross-tie

valves

upon

ESW header

low pressure

annunciation.

This. credit for prompt manual

operator action in order to restore

ESW to operable

was inappropriate

in that it had not been

previously established

as part of the licensing review of the

plant.

The rest of the evaluation supplied appropriate

justification that operability was established

without taking

credit for manual action.

CR 96-0127

With the reactor at full power, the Unit 2 containment jib crane

spilled hydraulic fluid into the reactor cavity during testing.

The prompt operability determination relied upon

a valid

engineering

judgement

argument,

however the backup operability

determination

also relied upon engineering

judgement.

Several

weeks after the backup operability was performed the licensee

performed

a reportability determination.

The reportability

determination

was more technical

in nature

and supported

the

prompt

and backup operability determinations.

A lack of engineering rigor was demonstrated

through the reliance

on engineering

judgement for both the prompt and backup

operabil'ity evaluations.

13

CR 96-0472

The Unit

1

AB D/G before

and after lube oil pump was found to have

its discharge

check valve improperly installed

such that it would

not have closed

when needed to prevent reverse flow.

This

condition was identified while the D/G was inoperable

and

corrected prior to restoring the D/G to operable.

No operability

determination

was required for operating

under this condition,

however

an operability determination

was required in order to

determine

past operability and thus reportability.

The licensee's

prompt operability determination

was

based strictly

on engineering

judgement.

Normally the backup operability

determination

would be expected to provide more engineering rigor,

however

none

was performed.

There

was

a reportability

determination

performed with much more detail than the prompt

operability determination

concerning the lube oil pump check valve

and failure modes,

however it too only contained

engineering

judgement.

A lack of engineering rigor was demonstrated

through the reliance

on engineering

judgement for both the prompt and backup

operability evaluations.

CR 96-0335

With the reactor at full power, the Unit 2 containment jib crane

spilled hydraulic fluid into the reactor cavity during testing.

Both the prompt and backup operability evaluations utilized only

engineering

judgement to assess

the acceptability of the oil in

reactor cavity or the reactor coolant system.

The backup

oper ability evaluation

assessed

post accident

environmental

conditions but did not address

the oil's interaction with nuclear

fuel or other internal reactor vessel

components.

Following the initiation of the refueling outage

several

weeks

later, the licensee realized that the operability determinations

did not address

the oil's affects

on refueling operations.

Another determination

was performed which did address

refueling

operations

but it too only relied upon engineering

judgement

and

did not specifically address

the oil's affect upon the fuel

bundles.

Again,

a lack of engineering rigor was demonstrated

through the

reliance

on engineering

judgement for both the prompt and backup

operability evaluations.

3)

Lar e Bore P'n

Reconstitution

Pro ram

LBPRP

and The

Identification of De raded

Pi

e

Su

orts

The inspectors identified one example of a licensee corrective action

program that had

been initiated prior to

GL 91-18 whose operability

determination

process

had not been modified after

GL 91-18 (the

LBPRP)

and this appeared

to affect the evaluation of degraded

pipe supports

identified through other mechanisms.

In the late 1980's licensee

and

NRC personnel

identified situations

where as-found piping and piping supports did not meet the original

FSAR

design requirements.

This was documented

in NRC inspection reports

and

licensee

documents.

The licensee

began

a program to identify, assess,

and where appropriate to correct these deficiencies.

The program was

committed to and documented

in correspondence

to the

NRC.

In licensee letter AEP:NRC: llOOA, issued

February

16,

1990, the licensee

committed that

"When these or similar reviews reveal

discrepancies

between

the as-found

and the as-designed

condition,

an evaluation of the

acceptability

and reportability of the condition is conducted."

The inspectors

determined that the licensee

was not in fact performing

specific calculations

on each identified discrepancy

or relying upon

bounding calculations

but was instead relying upon the results of series

of walkdowns in order to assess

operability of the supports.

The

walkdowns

had

been

performed

on

a sampling basis

and any identified

discrepancies

were evaluated

using interim acceptance criteria.

The

results of these

walkdowns were used to justify the operability of

safety related piping systems

in their existing configurations.

In teleconferences

with resident

inspectors

and Region III personnel,

the licensee

stated that licensee letter AEP:NRC:1100C,

dated

March 20,

1995,

documented this practice, that

NRC had been

a party to

teleconferences

in which this operability practice

had

been discussed

and that

NRC inspection reports

had accepted this practice.

A detailed

review of the referenced letter by the resident staff and

NRC region III

personnel

cognizant of this issue identified a reference to results of

the sample walkdowns being acceptable,

but no statement

could be found

which stated the licensee's

practice of only relying upon the walkdowns

for operability determinations

of discrepancies.

Interviews with NRC

piping exper ts

and their management

determined that none

remembered

any

such discussions.

A review of inspection report (50-315/316-91028)

showed that

a review of two systems

was indeed performed

and the

licensee's

operability determinations

were found to be acceptable.

However, the review was limited to just those

two systems

and the

acceptability

was also limited to just the discrepancies

identified on

those

two systems.

No blanket acceptability of the practice of relying

upon the walkdown samples

was meant or implied.

This was confirmed

during interviews with the lead

NRC inspector for the referenced

inspection report.

15

The

LBPRP was discussed

previously in inspection report 315/316-95012

and

an inspector follow-up item was issued

regarding resolution of the

licensee's

commitment to perform specific reviews

(50-315/316-95012-

02(DRP)).

This item will remain

open pending the assessment

of the

licensee's

response

to the request for information discussed

in the

cover letter.

Examples of piping support discrepancy

whose operability evaluation

appeared

not to meet

GL 91-18 are discussed

below:

CR 96-0395

During a walkdown on March 20,

1996,

a U-Bolt on 2-AFW-L944 was

found to not conform to the design drawing.

The prompt

operability determination relied upon

AEPSC Guideline 5700-13

which documents

the licensee's

operability determination practice

as discussed

above.

CR 94-1124

During an examination of a pipe support for an unrelated

reason,

on June 6,

1994, support

number 2-GC-R39 was found to not conform

to the design sketch.

The criteria contained within AEPSC

Guideline 5700-13

was relied upon for a prompt operability

determination.

CR 96-0180

During a walkdown with licensee

personnel

of the plant,

NRC

inspectors identified 14 discrepancies

on piping supports for

various safety related

and non-safety related

systems.

The

inspection

was documented in report 50-315/316-96003

(IPAP).

The

LBPRP was not intended

by the licensee to address

non-safety

related

systems,

but for those safety related support

discrepancies

identified by the inspectors

the licensee relied

upon the guidance

contained with AEPSC 5700-13.

The separate

issue of the timeliness of initiating CR 96-0180 is addressed

elsewhere

in this report

as

a Notice of Violation.

We were concerned that the operability assessments

performed

as

a part

of the

LBPRP and support discrepancies

identified through other

mechanisms

did not appear to comply with NRC Generic Letter 91-18.

A

request for a response

concerning the licensee's

operability assessments

for pipe supports

was discussed

on the front cover of this report.

c.

Conclusions

The licensee

generally failed to implement the timeliness guidelines of

GL 91-18 for performing operability evaluations.

In addition,

examples

of the quality of the operability evaluations

not meeting

GL 91-18 were

identified concerning piping support discrepancies.

A Notice of

Violation with three

examples

was issued for failing to meet licensee

16

procedural

requirements for timeliness.

A request for information

concerning the apparent

lack of piping supports to meet

Gl 91-18

requirements

was issued.

Issuance of A Re ort

Re uired

b

10 CFR Part 21 - Both Units

Ins ection

Sco

e

37551

The inspectors

performed routine followup activities in response

to

a

licensee

issued report required

by 10 CFR Part 21.

The inspectors

independently

assessed

the licensee's

operability assessment

for the

emergency diesel

generators

and the details contained within the Part

21

report.

Observations

and Findin s

Initial Identificati on of Failed

Com onent

On June

20,

1996, at 9:45

am

EDT the licensee called the

NRC

Headquarters

Operations Officer via the Emergency Notification System

and

made

a report

as required

by 10 CFR Part 21.

The licensee

reported

that

a failure of the, emergency diesel

generator

(D/G) cam follower

spring which occurred

on April 13,

1996, represented

a substantial

safety defect

and was reportable

under

10 CFR Part 21.

On April 13,

1996, Unit 2 was in a refueling outage with the reactor

defueled.

While troubleshooting for a speed control problem on the

2

CD

engine

a loud knocking was heard.

During followup to that knocking the

licensee

discovered that one cylinder had

a failure of its cam follower

spring.

The licensee

performed appropriate

followup activities and

identified one other broken spring on the

2

CD D/G.

One of the two broken springs resulted in its associated

cylinder in not

being able to produce

power.

The other broken spring was not as

severely

damaged

and its cylinder was still able to produce

power.

Licensee's Initial Root Cause

Anal sis

and Corrective Actions

The licensee

performed acoustic monitoring of the cylinders

on the other

three

D/Gs (two on Unit

1 and the other one

on Unit 2)

and did not

identify any other failed springs.

One spring

on the

2 AB D/G was

removed

and inspected

in response

to noise

on one cylinder,

however,

no

problems

were identified.

The licensee

had also observed that the set screws for the spring cover

plate

had

been

found loose

on the spring first identified as failed and

ensured that the other three

D/Gs had tight setscrews.

Licensee

management

had discussed

with the inspectors their bases for

three

D/Gs being operable following the April 13,

1996, failure.

This

basis for oper ability included all the information discussed

previously

in this section.

The

2

CD D/G was repaired

and tested prior to being

17

declared

operable.

The inspectbrs

had no significant concerns with the

licensee's

discussion

on their basis for operability.

Issuance

of A Re ort

Re uired

B

10 CFR Part 21

The licensee

determined that the D/G spring failure met Part

21

reporting requirements

on June

19,

1996.

The report was

made

on June

20,

1996.

This met the two day reporting requirements

of Part 21.

The

narrative

appeared

to meet the reporting requirements,

however it did

fail to supply important, pertinent information.

For example the

report:

~

Failed to discuss

the basis fot reportability (it represented

a

substantial

safety hazard).

~

Failed to discuss

the past

and current operability of the four

D/Gs in detail sufficient to inform the reader of the present

operability status of the D/Gs.

Failure to Document The Basis

For 0 erabilit

Following the issuance of the

10 'CFR Part

21 report discussed

above,, the

inspectors

attempted to review the licensee's

basis for operability for

the other three

D/Gs.

This review was to ensure that no new information

was revealed

in the Part

21 which invalidated the previous basis for

operability.

The licensee's

requirements

for performing operability

evaluations

was

implemented through Plant Hanagers

Instruction (PHI)-

7030, "Corrective Action" as

was discussed

in El.l.

CR 96-0622

was written on April 17,

1996, to document the failure of the

2

CD D/G cam follower springs.

This

CR did not contain

a prompt

operability determination required in PHI-7030

as it only addressed

2

CD

D/G and it had been declared

inoperable for maintenance

{thus it wasn'

required to be operable).

However the inspectors

could not locate

any

documented operability evaluation for the other D/Gs.

Subsequently

the

licensee

confirmed that no operability evaluation

had

been

documented.

The licensee

was required to perform and document

a prompt operability

evaluation for the remaining three

D/Gs following the spring failure on

April 13,

1996.

The licensee's

failure to comply with PHI-7030 is

a

violation {example {a) of 50-315/316-96006-01{DRP))

{this violation is

also discussed

in paragraph El.l.b. 1 above).

Conclusions

The licensee's

Part

21 report was accurate

but lacked certain desired

information.

The licensee failed to ensure that

an operability

evaluation

was documented

however this issue

was address

in El.l above.

18

E8

E8.1

Niscellaneous

Engineering

Issues

(92902)

Closed

I s ector Follow-u

Item 50-316 93020-02:

Loss of turbine

driven auxiliary feedwater

(TDAFW) pump flow retention

due to inaccurate

flow measurements.

This item concerned

the fact that the flow sensing

device which initiated a flow retention signal for the Unit 2 TDAFW pump

was reading only 78 percent of actual flow.

The instrument

inaccuracy

was corrected

by a modification, installed in 1994, which moved the flow

orifice to

a straight run of piping.

This modification eliminated

oscillations

and turbulence

across

the orifice which resulted in more

accurate

flow measurements.

The inspector reviewed the licensee's

post

modification tests to ensure that the flow instruments that initiated

a

flow retention signal

were accurately indicating actual

flow rates.

This item is closed.

E8.2

0 en

Inte rated

Pe formance Assessment

ro ram

IPAP

Issues

The inspectors

reviewed the

D. C. Cook Integrated

Performance

Assessment

(IPAP) Final Analysis

(NRC Inspection

Report Nos. 50-315/316-96003),

and identified inspection

issues

documented

by the

IPAP team.

Various

paragraphs

and

comments

were given individual item numbers.

Those item

numbers

which rose to the level of violations, unresolved

items, or

inspector follow up items are

so identified in the below list.

Some

items concerned

issues that were either the

same

item or were similar in

nature.

Those issues

are referenced

whenever possible in the list of

items below.

It should

be noted that the section

.numbers referenced

below are the section

numbers

from inspection report 50-315/316-96003

and are not from this inspection report.

Item No.

01

Condition reports

(CRs) were either not initiated or not done

so in a

timely manner.

(Section 1.1, "Safety Assessment

and Corrective Action")

Untimely identification and resolution of conditions adverse

to quality

is

a violation of 10 CFR 50, Appendix B, Criterion XVI "Corrective

Action."

(50-315/316-96006-02)

Specific examples

are addressed

in

other items below.

Three examples

were given; these

and others

are addressed

in more detail later

in the report:

01A

A CR was initiated 4 days after the team

and the system engineer

identified possible auxiliary feedwater

system piping support

deficiencies.

(Section 1.1)

See item 62.

01B

A CR was not initiated when licensee identified that boric acid

heat trace instrumentation,

used to verify compliance with TS

surveillance

requirements,

was not included in plant calibration

program.

(Section l. 1)

See

item 44.

19

02

03

04

05

" 06

07

08

09

10

12

01C

A CR was not initiated when foreign material

was found in interior

of feedwater heater level control valve 2-HRV-.651 during

maintenance

of the valve.

(Section

1. 1)

See item 60.

Documented operability determinations

were delayed.

(Section

1. 1)

See

paragraph

E. l.l.b.l of this report.

gA audits

and surveillance findings appeared

to be programmatic in

nature

and fairly narrow in scope.

(Section 1.1)

This issue

and item 12

are

an IFI. (50-315/316-96006-04)

CR causal

determinations

associated

with issues

not requiring

a formal

root cause

evaluation

were narrowly focused,

did not address

potential

generic aspects,

and contributed to inadequate

corrective actions.

(Section 1.2)

See

items 07 and 0&.

A large number of CRs were assigned

to generic root cause

categories,

which resulted in little trending value.

(Section 1.2)

This issue is

an

IF I. (50-315/316-96006-05)

Ferrography identified by lab analysis,

(EDG) governor oil sample

marginal

due to high particulate count. Subsequently,

the governor

failed due to contaminants

in oil.

(Section 1.2)

See item 77.

Corrective

actions taken in response

to identified plant problems

were

not always effective.

Problems recurred

due to inadequate

and/or timely

follow-up corrective actions.

(Section 1.3)

This is

a violation of 10 CFR 50 Appendix B, Criterion XVI, "Corrective Action." (50-315/316-

96006-02)

This includes item 08 below.

The specific examples

are

addressed

in other items.

Corrective actions

tended to be narrowly focused.

(Section 1.3)

This

is a portion of the issue identified in item 07.

Repeated

Component Cooling Water

pump discharge

check valve slamming

events

due to failure to install vendor recommended

stop plates.

(Section 1.3)

See item 48.

Unit 2 reactor/turbine trip due to actuation of moisture separator

reheater

high level switch.

Root cause

not determined.

(Section 1.3)

This issue

was reviewed in inspection report 50-315/316-95010.

Numerous foreign material exclusion control related

issues.

(Section

1.3 and 2.2)

The specific issues

were reviewed in inspections

reports.

See

item 75 for the general

issue.

Line organization

responses

to gA findings tended to be program oriented

and narrowly focused.

(Section 1.3)

See

item 03.

20

t

14

15

16

The team noted lack of programmatic controls that would preclude

subsequent

revision or elimination of the corrective actions

by the line

organization.'

(Section 1.3)

This issue is an IFI. (50-315/316-96006-

06).

Corrective actions associated

with rework CRs were narrow in scope.

Root cause

was not effectively determined

in several

cases

and

corrective actions to prevent recurrences

appeared

inadequate.

(Section

1.3)

See item 67.

Licensee's

response

to

NRC generic communications

were narrowly focused,

and relied upon actions already in place.

Licensee did not fully

address

the issues.

(Section 1.3)

This issue is an IFI. (50-315/316-

96006-07)

NRC Generic Letter 91-18 provided specific guidance for determining

operability of piping with degraded

supports.

The licensee did not

incorporate

any of the

GL 's specific guidance into existing programs.

(Section 1.3)

This issue is discussed

in section

E. 1. l.b.3 of this

report

and is being tracked

by IFI 50-315/316-95012-02.

OPERATIONS

17

19

20

21

Inconsistencies

between the functioning of the five operating

crews were

noted.

(Section 2.1)

This issue is an IFI. (50-315/316-96006-08)

Administrative activities were distracting shift supervision

from their

oversight responsibilities.

(Section 2. 1) This,issue is an IFI. (50-

315/316-96006-09)

Technical

operating guidance

was promulgated to shift supervisors

without indication that it had operations

management

approval for

implementation.

(Section 2.1)

This issue is an IFI. (50-315/316-96006-

10)

Lack of a questioning attitude

was observed

in some operators.

(Section

2. 1)

This was based

on limited observations

by the team,

and is an

element normally reviewed during routine operations

inspections.

No

further tracking is required.

Elevated

EDG lube oil temperatures

were identified in an August

1994

gA

audit, but had not been effectively corrected.

(Section 2. 1)

See item

03.

22

23

Cumbersome

nature of the work control

system did not facilitate

effective control of the status of other equipment.

(Section

2. 1)

This

issue is

an IFI. (50-315/316-96006-11)

See

items

34 and 55.

Operations

management

and supervision rarely used

gA assessment

or trend

results.

(Section 2.2)

See

items

03 and

05 regarding the weaknesses

in

gA assessments

and corrective action trending.

21

25

26

27

28

Correction of some longstanding deficiencies

such

as procedure

inadequacies,

work practices,

and equipment

clearance

errors

was

ineffective. 'Section 2.2)

The licensee's

action to address

these

concerns will be tracked under their response

to violation 50-315/316-

96006-02.

Specific examples

are addressed

in other items of this

report.

Despite procedure

changes,

performance

problems with inadequate

control

of Reactor Coolant System draining.

{Section 2.2) This issue is an IFI.

(50-315/316-96006-12)

Instances

of operators'ot

responding

promptly to alarms.

(Section

2.3)

This was

based

on limited observations

by the team,

and is an

element normally reviewed during routine operations

inspections.

No

further tracking is required.

Weaknesses

in system

knowledge in a few operators.

(Section 2.3)

This

issue

was addressed

in the inspection report reviews of specific events

and was

a comment

on minor discrepancies

observed

by the team.

Observation of new fuel receipt

and inspection revealed

instances

of

weak work practices.

(Section 2.3) This issue is an IFI. (50-315/316-

96006-13)

29

31

32

33

34

Recent inspection reports

and the team's

observations

indicated that

coordination

and communication with other site groups

was often

ineffective.

(Section 2.3)

This is an element normally reviewed during

routine operations

inspections.

No further tracking is required.

Many normal operating

and surveillance

procedures

were of lesser

quality.

(Section 2.4)

See

items

31

and 33.

The overall quality of administrative

procedures

also varied greatly.

(Section 2.4)

See

items 30 and 33.

Poor cor rective action was taken in response

to problems with poor

procedures.

(Section 2.4)

The role of specific procedures

in specific

events

was reviewed in inspection reports.

This issue is another

example of lack of adequate

corrective action which was

a violation of

10 CFR 50, Appendix B, Criterion XVI,

Corrective Action." addressed

with specific examples

in other items of this report.

Slowed implementation of procedural

improvements.

{Section 2.4)

Items

30, 31,

and

33 are

an IFI. (50-315/316-96006-14)

Both the work control

and the clearance

control processes

were

cumbersome,

imposing

a burden

on the unit supervisors.

(Section 2.4)

See

item 22.

35

Cryptic equipment

nomenclature

made work schedule readability difficult

(i.e., poor human factoring).

(Section 2.4)

See

item 22.

22

Scheduling

system did not easily support adjusting work activity

schedules if difficulties arose with a job.

(Section 2.4)

See item 22.

Unit supervisors'dministrative

burden

was increased

with multiple work

schedules

containing similar information.

(Section 2.4)

See

item 22.

ENGINEERING

38

39

40

41

Hanagement

involvement was not evident in the handling of deficiencies

identified by the "As Found Reportable"

(AFR) program.

(Section 3.1)

This issue is related to the effectiveness

of the corrective action

process

addressed

in item 07 and violation 50-315/316-96006-02.

Hanagement

involvement was not evident in the handling of

operability/reportability of the auxiliary feedwater

(AFW) pump

instantaneous

overcurrent trips.

(Section 3.1)

This issue is related

to the effectiveness

of corrective actions

addressed

in item 07 and

'iolation 50-315/316-96006-02.

The "As Found Reportable"

program was intended to identify Technical

Specifications related instruments

not in the calibration program. At

some date prior to January

1996, the licensee

had identified that TS-

related boric acid system temperature

instruments

were not in the

calibration program and,

as of February

5,

1996,

a condition report

(CR)

had not been written.

{Section 3.1)

Once this was noted

by inspectors,

a condition report

was not initiated until two days later.

Failure to

enter this deficiency in the corrective action program was

an example of

a violation of 10 CFR 50, Appendix B, criterion XVI. "Corrective

Action." which required that conditions adverse to quality promptly

identified and corrected.

= (example

(a) of 50-315/316-96006-02)

In two instances,

the Corrective Action Group

(CAG) incorrectly

designated

CR 95-1204 for the safety-related

motor-driven auxiliary

feedwater

pump

{HDAFW) motor

as not safety related.

(Section 3.1)

This

issue is addressed

with item 42.

Inspection report 50-315/316-95010

section 3.5 identified that the Unit

1 west motor-driven auxiliary feedwater

pump

(HDAFWP) had

a history of

instantaneous

overcurrent trips.

The

IPAP team noted that the

overcurrent protection circuit tripped the

pump within the design

operating

range of the bus voltage,

thus there

was

a possibility for the

pump to trip at any time when required to start,

during normal operation

or an accident condition.

(Section 3.1)

Only one

pump of three

(another

50 percent capacity motor-driven

pump

and

a

IOOX capacity

turbine-driven

pump)

was affected

by the

pump trip point at

approximately

4285 volts on

a nominally rated

4160 volt bus.

The effect

of this condition on pump and system operability is

an unresolved

item

(50-315/96006-15)

pending further

NRC review.

23

Delayed

and narrow-focused

use of the condition reporting process to

identify/capture

problems

was considered

a weakness.

Example:CRs

relating to a

CCW system temporary modification (TM).

(Section 3.2)

See

items

07 and 51.

The licensee did not promptly initiate condition reports to document the

various problems,

(ie)

CRs written for boric acid system high

temperatures

and uncalibrated

instrumentation

were written two days

after the issue

were identified.

(Section 3.2)

The timeliness of

documented operability determinations

was also influencing and

influenced

by the timing of CR initiations. It appeared

that the

initiation of a

CR was being delayed until

a formal documented

operability determination

could be prepared,

leaving the immediate

operability issue

unaddressed

in the interim.

Prompt identification of

a condition adverse to quality was

a requirement of 10 CFR 50, Appendix

B, Criterion XVI, "Corrective Action," which stated,

in part, that

conditions

adverse to quality are to be promptly identified and

corrected.

The failure to initiate corrective action in the past

and to

promptly initiate a condition report once these

issues

were identified

by the inspectors

were examples of a violation of 10 CFR 50 Appendix

B

(50-315/316-96006-02).

The issue of the uncalibrated boric acid system

temperature

instruments is 'addressed

in item 40.

The high temperature

issue is addressed

in item 45.

0

46

48

A condition report for the boric acid system high heat trace

temperatures

adverse

condition had not been written by operations

or

engineering until two days after inspectors

questioned

the system

status.

The high temperature

alarm condition of the temperature

instruments

could have

been identified on previous periodic operator

rounds.

(Section 3.2)

Failure to take prompt corrective action for a

condition adverse to quality was

an example of a violation of 10 CFR 50,

Appendix B, Criterion XVI, "Corrective Action," which required that

conditions adverse to quality be promptly identified and corrected.

(example (c) of 50-315/316-96006-02)

Unit

1

CCW flow balance surveillance did not meet the Updated Final

Safety Analysis Report

(UFSAR) 240

gpm minimum flows listed on

UFSAR

table 9.5-2 for sample coolers.

(Section 3.2)

The Unit

1 flow balance

procedure

EHP 4030 ST0.248 completed

on 9/28/95 listed

an objective to

achieve

195 gpm flow to the sample coolers.

The recorded

combined flows

of sample coolers

and the blowdown cooler flow was

142 gpm.

This item

is an IFI (50-315/316-96006-03).

Weaknesses

were also noted in the area of problem resolution.

Several

recurring issues

were not resolved in a timely manner.

(Section 3.2)

The specific issues

have

been reviewed in previous inspection report 50-

315/316-95010.

No additional inspector follow-up action

was required.

CCW check valve slamming root cause

not addressed.

Failure to resolve

the slamming issue in a timely manner

and failure to address

the

implementation of vendor

recommendations

were considered

to be

a

weakness

with the licensee's

resolution of the check valve slamming

24

50

51

issue.

(Section 3.2)

This issue

was addressed

in NRC inspection report

50-315/316-95010.

Hotor Driven

AFW Pump instantaneous

over current trips narrowly

addressed.

The narrow scope of the corrective actions

was considered

a

weakness

in the resolution of this issue.

(Section 3.2)

See item 42.

The inspectors

reviewed the licensee's

operability determination for

high temperatures

on the boric acid system.

Based

on missing

temperature profile data,

missing

NPSH calculations,

a lack of basis for

adequate

pressure

in the line to prevent boiling and the lack of

discussion of the high temperature effect on the process fluid, the

operability determination

was considered

to be inadequate.

(Section

3.3)

The inspectors

concluded that the system

was operable;

no further

inspector follow-up action is required.

The quality of the licensee's

operability determinations

is discussed

further in section E.l.l.b.2 of

this report.

Inspectors

reviewed the installation of a "Cosmos"

system analysis

apparatus

controlled by a

CCW system temporary modification (TH).

Several deficiencies

were identified with the TH.

(Section 3.3)

The safety evaluation failed to address

the effect of flow

through the equipment

on the overall

CCW flow balance.

Flow

balance

values

were listed in the

UFSAR.

The TH redirected

approximately

10 gpm from the other sample coolers including post-

accident

sample stations.

The total

CCW flow to the sample

coolers

was already less than described

in the

UFSAR.

See item

46.

The use of tygon tubing connections

was not specified in the

TH

and its design requirements

were not evaluated.

The licensee

initiated

CR 96-0179 for this issue.

The tubing was replaced with

tubing of a higher pressure/temperature

rating.

No further action

was required,

the safety evaluation did address

the potential

consequences

of a leak.

Review by the Plant Nuclear Safety Review Committee

(PNSRC)

was

marked

"N/A" although requirements

specified that when

a procedure

was initiated which had

a full safety evaluation,

PNSRC review was

required.

The licensee initiated condition report

CR 96-0210

and

issued revision

2 to procedure

PHP 1040.SES.001

to clarify the

requirements for PNSRC reviews.

No further action was required.

Following installation, but prior to placing

a TH in operation,

the completed

package

was required to be returned to the

control

room and placed in the

TH log.

The unit had been in

service for about 30 days,

however, the package

had not been

returned to the control

room,

and operators

were not aware that

the unit was in service.

This did not meet the requirements

of

the temporary modification procedure

PHP 5040 HOD.001;

however,

no

condition report was written to address this issue.

This was

25

52

53

another

example of a violation of 10

CFR Appendix

B for the prompt

identification and correction for a condition adverse to quality.

(50-315/316-96006-02)

Some weaknesses

were noted in that system engineers

were not reviewing

work requests.

(Section 3.4)

This was

a comment

on engineering

performance

which may be reviewed under normal inspection activities.

No further follow-up tracking required.

Other programs that warranted further review included post maintenance

testing which was to receive substantially

reduced

engineering

review

beginning in April 1996, fer rography (lube analysis)

program which was

not fully established

at the time of the onsite

assessment,

and the

backlog of modification package

indicated in the performance trend

report.

(Section 3.4)

Post maintenance

testing

was addressed

in

violation 50-315/95009-03.

The implementation of the ferrography

program was addressed

under IFI 50-315/94018-02.

The backlog of

modification packages

is an IFI (50-315/316-96006-16).

The team noted

few self assessment

activities were ongoing or planned in

the engineering

area.

(Section 3.4)

This was

a comment

on engineering

performance

which may be reviewed under normal inspection activities.

No further follow-up tracking required.

Boric Acid surveillance

procedure

12

OHP 4030.STP.023

was considered

weak because it did not provide acceptance criteria for maximum system

temperatures

or guidance

on what to do.

(Section 3.4)

This issue is

an

IFI. (50-315/316-96006-17)

CCM flow balance surveillance,

I-EHP 4030 STP.248

was considered

to be

weak because

the "Acceptance Criteria" data sheet did not contain the

sample coolers

and the data sheets

did not list acceptance criteria.

(Section 3.4)

See

item 46.

MAINTENANCE

57

58

59

Voluntary

LCO entries frequently exceeded their estimated

time for the

system to be returned to service.

(Section 4. 1)

This issue

was covered

under

URI 50-315/316-94022-02.

The corr ective maintenance

wor k backlog

had steadily risen

and

had

approximately doubled since

March 1995.

(Section 4. 1)

This was

a

comment

on the performance of maintenance

which may be reviewed under

normal inspection activities.

No further follow-up tracking required.

The time for "completion of a prio'rity 30" maintenance activity had

increased significantly.

(Section

4. 1)

This was

a comment

on the

performance of maintenance

which may be reviewed under normal inspection

activities.

No further follow-up tracking required.

26

61

62

63

The team was concerned with the licensee's

failure to recognize the need

to initiate a condition report to evaluate the as-found

damage of

secondary

valve 2-HRV-651 internals

and the presence

of foreign material

in the system.

(Section 4.2)

This is another

example of weakness

in

reporting conditions

as discussed

in item 44.

Equipment

had

been returned to service without an evaluation of the

foreign material

in the system.

(Section 4.2)

See item 75.

Piping support deficiencies.

The team considered

the licensee's

failure

to recognize

the need to promptly initiate condition reports to be

a

weakness.

(Section 4.2)

This issue is another

example of the issue

discussed

in item 44 and is considered

a violation of licensee

procedures

(example

(b) of 50-315/316-96006-02).

The team was concerned with the licensee's

timely completion of

oper ability determinations.

(Section 4.2)

This issue

was discussed

in

item 44.

The maintenance

department

was not effective at preventing the

recurrence of previously identified deficiencies.

(Section 4.2)

See

item 7.

The team identified a rework condition on the turbine room sump

pump,

12-PP-25-1,

that had not been identified by the licensee.

(Section 4.2)

See item 66.

67

Weaknesses

existed in the licensee's

process for identifying rework.

(Section 4.2)

This issue is an IFI. (50-315/316-96006-18)

The majority of condition reports written for rework were narrow in

scope

and were not effective at determining the root cause for the

rework or identifying appropriate

preventive actions.

(Section 4.2)

See item 66.

68

69

Maintenance

department self-evaluations

were programmatic

and were not

in-depth or critical.

(Section 4.2)

This was

a comment

on the

performance of maintenance

which may be reviewed under normal inspection

activities.

No further follow-up tracking required.

The team was concerned with the licensee's

apparently

high threshold for

the identification of material condition problems.

(Section 4.3)

See

item 44.

70

The team

was concerned with the licensee's

lack of timeliness with

initiating condition reports

when appropriate.

(Section 4.3)

See item

44.

71

U-1

W centrifugal charging

pump was found to be inoperable

from March

15,

1996 through September

12,

1995.

(Section 4.4)

This item was

addressed

in violation 50-315/95014-01.

27

~lt

?3

74

75

76

77

U-1 main transformer

was

damaged

on July 16,

1995,

due to the improper

installation of a main generator

voltage potentiometer.

(Section 4.4)

This issue

was previously discussed

in NRC inspection report 50-315/316-

95009.

No further review is required.

U-1 East motor driven auxiliary feedwater

pump was damaged

on December

30,

1994,

as

a result of inadequate

maintenance.

(Section 4.4)

This

item was tracked

by LER 94015.

The team was concerned that licensee

management

appeared

not to have

recognized

commonalities

between

the causes for the events

discussed

in

items 71, 72,

and 73.

This issue will be addressed

in item 71, in

response

to violation 50-315/95014-01.(Section

4.4)

The foreign material exclusion practices

was considered

a weakness.

(Section 4.4)

This issue is an IFI. (50-315/316-96006-19)

See

item 61.

The licensee failed to replace

EDG quick exhaust

valve diaphragms

at the

scheduled interval.

(Section 4.5)

This issue is an IFI. (50-315/316-

96006-20)

The team considered

the ferrography program ineffective.4.5

This issue

was tracked

by URI 94-018-02 which is here re-designated

as

an IFI.

78

Procedural

adherence

or inadequate

maintenance

procedures

were

identified as contributing causes

to equipment failures by both the

NRC

and the licensee.

(Section 4.5)

This issue is an IFI. (50-315/316-

96006-21)

See item 74.

PLANT SUPPORT

79

80

81

Inadequate

management

involvement to address

the

number of unnecessary

alarms.

(Section

5. 1)

This issue

was reviewed in inspection report 50-

315/316-96004

under open item IFI 50-315/316-95012-03

The

PASS continued to have material condition deficiencies. (Section 5.2)

This issue

was reviewed further in inspection report 50-315/316-96004.

PASS

gC records

revealed significant weaknesses

in the program

implementation.

(Section 5.2)

This issue

was further reviewed in

inspection report 50-315/316-96004

and

a violation 50-315/316-96004-02

was issued.

82

83

Weaknesses

were evident in the chemistry staff's ability to identify and

resolve performance

issues.

(Section 5.2)

This issue

was further

reviewed in inspection report 50-315/316-96004

and

a violation 50-

315/316-96004-02

was issued.

1995 exercise

weakness

(verbal

communication).

Indicating

a lack of

issue resolution.

(Section 5.2)

This issue

was further reviewed in

inspection report 50-315/316-96004

under open item IFI 50-315/316-95007-

02.

28

ll

84

Improper donning of protective clothing.

(Section 5.3)

The report

identified isolated occurrences

noted

as

an indicator of level of

performance.

- Additional inspection of this area

was documented

in

inspection report 50-315/316-96004.

85

Chemistry technicians

(CTs) did not perform radiation surveys of reactor

coolant system

(RCS)

samples

or sample

areas

during routine sampling.

The reliance of an

ED as

a survey instrument

was considered

a weakness.

(Section 5.3)

This issue is an IFI. (50-315/316-96006-22)

86

Boron samples

(November

and December

1995) required

by

PASS

gC

procedures

were discarded

by the chemistry department

before their

analyses.

(Section 5.3)

This issue

was further reviewed

and violation

50-315/316-96004-02a

was issued.

87

Boron analytical

comparisons for September

1995 were not properly

documented.

(Section 5.3)

This issue

was further reviewed

and

violation 50-315/316-96004-02a

was issued.

88

The licensee failed to take required action when the acceptance

criteria

in 12 THP 6020

PAS.016 were not met.

(Section 5.3)

This issue

was

further reviewed

and violation 50-315/316-96004-02b

was issued.

29

A

Licensee

  • A
  • K
  • D
  • T
  • f
  • J
  • B
  • H
  • p
  • D
  • J
  • C
  • H.
  • l

"A.

  • p

IP 37551

IP 61726

IP 62703

IP 71707

~oened

PARTIAL LIST OF

PERSONS

CONTACTED

Blind, Site Vice President

Baker, Assistant Plant Hanager

Noble, Radiation Protection Superintendent

Postlewait,

Site Engineering Support

Hanager

VanGinhoven, Haterial

Hanagement

Department

Allard, Haintenance

Superintendent

Gillespie, Operations

Superintendent

Hierau, Operations

Shift Technical Advisor Supervisor

Schoepf,

Supervisor,

Safety Related

Systems

Horey, Chemistry Superintendent

Kobyra, Hanager Nuclear Engineering

Freer,

Scheduling

Depuydt,

Licensing

guaka,

Project Hanagement

& Inst. Services

Barker, Plant Performance

Assurance

Russell,

Plant Protection

INSPECTION

PROCEDURES

USED

On-site Engineering

Surveillance Observations

Haintenance

Observation

Plant Operations

ITEHS OPENED,

CLOSED,

AND DISCUSSED

50-315/316-96006-01

50-315/316-96006-02.

50-315/316-96006-03

50-315/316-96006-04

50-315/316-96006-05

50-315/316-96006-06

VIO

Failure to perform a prompt operability

assessment

VIO

Failure to identify 10CFR50 Appendix

B Criterion

XVI "corrective actions" in a prompt manner.

IFI

No written 10 CFR 50.59 evaluation.

IFI

gA audit and surveillance findings appeared

to

be programmatic

and narrow in scope.

IFI

A large number of CR's were assigned

generic

root cause categories,

therefore of little

trending value.

IFI

No programmatic control to preclude revisions or

elimination of corrective actions.

I

30

0

50-315/316-96006-07

IFI

Responses

to

NRC generic communications

was

narrowly focused

and did not fully address

the

issues.

50-315/316-96006-08

50-315/316-96006-09

50-315/316-96006-10

50-315/316-96006-11

50-315/316-96006-12

50-315/316-96006-13

50-315/316-96006-14

50-315/316-96006-16

50-315/316-96006-17

50-315/316-96006-18

50-315/316-96006-19

50-315/316-96006-20

IFI

IFI

IFI

IFI

IFI

IFI

IFI

IFI

IFI

IFI

IFI

IFI

The operating

crews did not function the same.

Administrative activities were distracting shift

supervision

from their oversight

responsibilities.

Technical

operating guidance

was promulgated to

shift supervisors

without indication that it had

operations

management

approval for

implementation.

Cumbersome

nature of the work control

system did

not facilitate effective control of the status

of other equipment.

Despite procedure

changes,

performance

problems

with inadequate

control of Reactor Coolant

System draining.

Observation of new fuel receipt

and inspection

revealed

instances

of weak work practices.

Slowed implementation of procedural

improvements.

Post maintenance

testing which was to receive

substantially

reduced

engineering

review

beginning in April 1996, ferrogr aphy (lube

analysis)

program which was not fully

established

at the time of the onsite

assessment,

and the backlog of modification

packages

in the performance trend report.

Boric Acid surveillance

procedure

12

OHP

4030.STP.023

was considered

weak because it did

not provide acceptance criteria for maximum

system temperatures

or guidance

on what to do.

Weaknesses

existed in the licensee's

process for

identifying rework.

The foreign material

exclusion practices

was

considered

a weakness.

The licensee failed to replace

EDG quick exhaust

valve diaphragms

at the scheduled

interval.

31

G

~

'

50-315/316-96006-21

IFI

Procedural

adherence

or inadequate

maintenance

procedures

were identified as contributing

causes

to equipment failures by both the

NRC and

the licensee.

50-315/316-96006-22

IFI

The reliance of an

ED as

a survey instrument

was

considered

a weakness.

50-315/94-018-02

Closed

IFI

URI (same

number) re-designated

as

a IFI.

50-316/93020-02

IFI

Loss of turbine driven auxiliary

feedwater(TDAFW)

pump flow retention

due to

inaccurate

flow measurements.

DISCUSSED

50-315/96006-15

UDI

Inspection report 50-315/316-95010

section 3.5

identified that the Unit

1 west motor-driven

auxiliary feedwater

pump

(HDAFWP) had

a history

of instantaneous

overcurrent trips.

The

IPAP

team noted that the overcurrent protection

circuit tripped the

pump within the design

operating

range of the bus voltage,

thus there

was

a possibility for the

pump to trip at any

time when required to start,

during normal

operation or an accident condition.

32