ML17325A660

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Safety Insp Repts 50-315/88-03 & 50-316/88-04 on 880111-14,25-28 & 0302.Violation Noted.Major Area Inspected: Licensee Actions on Previously Identified Items & LER Followup
ML17325A660
Person / Time
Site: Cook  American Electric Power icon.png
Issue date: 03/08/1988
From: Darrin Butler, Gardner R, Ulie J
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17325A658 List:
References
50-315-88-03, 50-315-88-3, 50-316-88-04, 50-316-88-4, NUDOCS 8803150375
Download: ML17325A660 (15)


See also: IR 05000315/1988003

Text

U ~ S.

NUCLEAR REGULATORY COMMISSION

REGION III

Reports

No. 50-315/88003(DRS);

50-316/88004(DRS)

Docket Nos.

50-315;

50-316

Licensee:

Indiana Michigan Power

Company

1 Riverside

Plaza

Columbus,

Ohio

43216

Licenses

No.

DPR-58;

DPR-74

Facility Name:

D.

C.

Cook Nuclear Plant, Units 1 and

2

Inspection At:

AEPSC,

Columbus,

Ohio and

D.

C.

Cook Site,

Bridgman, Michigan

Date

Inspection

Conducted:

January

11-14, 25-28,

and March 2,

1988

Inspectors:

D.

S. Butler

Date

J.

M. Ulie

3

8'pproved

By:

R.

N. Gardner,

Chief

3 9

Plant Systems

Section

Date

Ins ection

Summar

Ins ection on Januar

11-14

25-28

and March 2

l988

Re orts

No. 50-315/88003

DRS

.

No. 50-316/88004

DRS

Areas Ins ected:

Special

announced

safety inspection of

on previously identified items

and Licensee

Event Report

inspection

was performed in accordance

with IE Procedure

Results:

Of the areas

inspected,

one apparent violation

(Failure to implement adequate

design control measures-

3.a(2),

and 3.b(1)).

licensee

actions

followup.

The

92700

and 92701.

was identified

Paragraphs

3. a(l),

8803150375

880308

PDR

ADQCK 05000315

6

PDR

DETAILS

1.

Persons

Contacted

Indiana

and Michi an Electric

Com an

Personnel

"W. Smith, Jr., Plant Manager

"A. Blind, Assistant Plant Manager - Administration

  • J. Rutkowski, Assistant Plant Manager

Production

  • B. Svensson,

Licensing Activity Coordinator

"T. Bei lman, I 8 C/Planning Superintendent

  • T. Postlewait,

Technical

Superintendent

- Engineering

"C. Ross,

Compute'r Science

Superintendent

  • J. Droste,

Maintenance

Superintendent

"S. Delong, I 8

C Production Control General

Supervisor

"D. Krause,

I 8

C Production Supervisor

J. Wojoik, Chemical Supervisor

R.

Hennen,

Nuclear Section

Head

  • T. Langlois, I & C Production Control

"G. Arent, .Operations

"B. Stoner,

Computer

Science

B. Burgess,

Training

AM. Barfelz, Safety

and Assessment

American Electric

Power

Service

Com an

Personnel

M. Alexich, Vice President,

Nuclear Operations

+B. Auvil, Nuclear Safety

and Licensing

+iP. Barrett,

Manager,

Nuclear Safety

and Licensing

+R. Carruth,

Manager, Electrical Generation

Section-N

R.

Kroeger,

Manager,

equality Assurance

+B.

Lauzau,

Nuclear Safety and Licensing

(NS 8 L)

R. Vassey,

NS

8

L

R. Kraszewski,

NS

8

L

K. Toth,

NS

8

L

R.

Shoberg,

Mechanical

Engineering Division - I 8

C

W. Sotos,

Mechanical

Engineering Division -,I 8

C

J.

Anderson, Electrical Generation

Section -

N

D. Maxwell, Nuclear Operations

Division

C. Erikson, Nuclear Operations Division

G. John,

Nuclear Fuels

and Analysis

"R. Huerter,

Supervisory Auditor - gA

NRC Personnel

"B. Jorgensen,

Senior Resident

Inspector

~J. Heller, Resident Inspector

  • Denotes

those attending the exit meeting

on January

28,

1988.

~ Denotes

those attending the telecon meeting

on February 3,

1988.

+ Denotes

those attending the telecon exit meeting

on March 2,

1988.

The inspectors

also contacted

other personnel

during the course of the

inspection.

2.

Licensee Action on Previous

Ins ection Findin

s

92700

and

92701

a.

b.

(Closed) Part

21 Item (315/78001-PP;

316/78001-PP):

Deficiencies

in environmental qualification of Cutler-Hammer

(C-H) terminal

blocks.

The terminal blocks, if used,

were found inside containment

and were

housed in penetration

terminal

boxes.

The licensee

removed all leads

from any

C-H terminal blocks

and spliced the

leads

together with qualified (40 years)

Raychem splices

and

terminations.

Procedure

12

THP 6030

IMP. 071, "Instrument and

Control Environmental gualification of. Safety Related Electrical

Equipment Surveillance/Maintenance

and Replacement

Program,"

recommended

adequate

surveillance

and maintenance activities to

ensure that electrical control,

power and instrumentation

cables

and terminations that were

Eg would retain their environmental

qualification.

(Closed) Part

21 Item (315/81001-PP;

316/81001-PP):

Possible

failure of Volume Control Tank (VCT) level instrumentation.

Westinghouse

identified the potential for the

VCT level controller

(gLC-452) to fail high due to a failure of the controllers capillary

reference

leg.

The

VCT low level alarm (5 inches)

was fed from

gLC-452.

Without reactor operator intervention the

VCT could empty

with a loss of suction to any operating centrifugal charging

pump

(potential to damage

the pumps).

A single

random failure in the

VCT

level control

system could lead to a loss of redundancy

in the high

head safety injection system.

The licensee

added

an additional

VCT low level alarm (10 inches)

for both units.

Procedures

1-OHP 4024. 109 and

2-OHP 4024.209,

"Annunciator ¹9 Response

Boric Acid," were modified and contained

adequate

instructions

on how to respond to VCT level annunciators.

In addition, operator

lesson plan RO-C-E507,

"Basic Control

Systems,"

was modified to include information on instrument

reference

legs

and the effects of their failure on instrumentation.

(Clos'ed) Part

21 Item (315/81002-PP;

316/81002-PP):

Deficiencies

in Eberline micro-computer

based radiation monitoring equipment.

There was

a potential error in the interrupt structure of the

central processing unit (CPU III) board.

Two interrupts of

increasing priority that occur sequentially

could cause

the

interrupt data to be lost.

The vendor supplied the licensee with vendor manual

procedure

inserts

and modification kits for the following equipment:

~ PT-1

~ CT-1

~ Sping-3/Sping-4

I

Portable

Terminals

Control Terminals

Particulate,

Iodine and Noble Gas Monitors

All the modifications were completed

and tested satisfactorily.

The inspectors verified that all the controlled manuals

had the

insert attached

to the

CPU III manual section at American Electric

Power

(AEP) and at the plant.

Only one manual

(Sping-3/Sping-4)

in the Instrument

and control Satellite Library, at the plant, did

not contain the insert.

The licensee

promptly removed the manual

from circulation and issued

paperwork to have

a controlled copy of

the insert placed in the manual.

The guality Assurance

(gA)

organization

committed to perform a surveillance of all plant

satellite libraries during their current on-going audit.

This item appears

to be an isolated

case

and the inspectors

have

no further concerns

in this area.

d.

(Closed) Part

21 Item (315/82001-PP;

316/82001-PP):

Brown-Boveri

Electric/ITE low voltage circuit breaker solid state trip devices

have

an electrolytic capacitor which could potentially fail and

prevent the trip unit from opening the breaker.

Subsequent

licensee

investigation determined that the capacitor

had

a low failure rate

and that immediate

change

out of all the trip units did not

constitute

a significant safety hazard.

The licensee

has

changed

out some of the trip units, modified an

existing Type 504 breaker test set

and purchased

a new 504 test

set.

The .504 test set

can detect

a failing capacitor.

The

inspector

reviewed Procedure

12

MHP 5021.082.010,

"Maintenance

Calibration Procedure

For Trip Devices,

Types

SS-13

and SS-14

used

on 480V and

600V Power Circuit Breakers,"

and determined that there

were adequate

procedure

steps

and acceptance

criteria to detect

a

failing capacitor.

e.

(Closed) Part

21 Item (315/83002-PP;

316/83002-PP):

Static

.calibration drift of zero suppressed

Model 763 Barton pressure

transmitters.

These transmitters

were supplied

by Westinghouse

to

measure

pressurizer

(PZR) pressure.

The potential

magnitude of the

drift between in-plant calibrations

(18 months)

was established

as

4.2 percent

and always in the negative direction.

The licensee

replaced

the

PZR pressure

transmitters with new Eg Foxboro Units in

1985 for Unit One and

1986 for Unit Two.

The inspector

reviewed the past two Barton calibrations, prior to

their change out,

and determined that the maximum drift experienced

was within each units safety analysis.

In addition, transmitters

that were exhibiting a larger drift were calibrated

more frequently

and analyses

were performed to address

channel operability.

None of

the transmitters

experienced

a 4.2 percent drift.

(Closed) Part

21 Item (315/84001-PP;

316/84001-PP):

Undetectable

test switch failure in the Westinghouse

Solid State Protection

System

(SSPS).

A momentary pushbutton

(PB) test switch was

used to

test the continuity path through the safeguards

slave relay.

The

PB

would energize

the master relay and open contacts that were shorting

out the logic test

lamp.

Failure of the

PB contacts

to close

and

short out the test

lamp would place the test

lamp in series with the

slave relay coil.

On a safeguard activation, failure of the

lamp

would prevent the slave relay from actuating

safeguard

equipment.

The licensee

has adequately

modified the test circuitry and

procedures

1 THP 4030 STP.410,

1 THP 4030 STP.411,

2 THP 4030 STP.510,

and

2 THP 4030

STP! 511 (Reactor Trip SSPS

Logic and Reactor Trip

Breaker Train A(B) Surveillance Test (Monthly)) to detect

a test

switch failure.

(Closed) Part

21 Item (315/84002-PP;

316/84002-PP):

Brown-Boveri

Electric/ITE low voltage circuit breaker solid state trip devices

have silicon controlled rectifiers

(SCR) that could exhibit high

leakage current.

The excessive

leakage current

may cause'mproper

operation of the trip device.

The vendor

recommended

a special

stress

test

be used to detect

bad

SCRs.

The licensee

has incorporated

the vendors

recommended

testing in

procedure

12

MHP 5021.082.010.

The procedure

steps

and acceptance

criteria were adequate.

(Closed) Part

21 Item (315/84005-PP;

316/84005-PP):

Deficiency in

the

DETECTOR computer

code that is used to calculate

the Technical

specification

(TS) limits for enthalpy rise peaking factors.

The

DETECTOR code

was previously reviewed in NRC inspection report 87028.

The report closed out

LER 84007 and

Open Item 84014-01

on licensee

implemented corrective actions to ensure

the adequacy of the

DETECTOR code.

The inspector further reviewed the application of the process

computer

(P250) for providing acceptable

plant data to support

TS

calculations.

The

DETECTOR code

uses real-time plant data that is

processed

by the

P250 computer.

The licensee calibrates

the process

parameter

voltage to frequency (V/F) converters that input to the

P250

on an 18 month interval.

The

P250 verifies the adequacy of,

the information it receives

by using internal diagnostic

programs.

A diagnostic error is generated

when

a V/F converter is out of

specification.

The

DETECTOR code

uses its own diagnostic

programs

to determine

the adequacy of the data received

from the P250.

The inspector

has

no further concerns

in this area.

(Closed) Part

21 Item (315/86001-PP;

316/86001-PP):

Instrumentation

error in the analog version of Reactor Vessel

Level Instrumentation

System

(RVLIS) used at non-upper

head injection plants.

The

Westinghouse

supplied

RVLIS system is used to provide accurate

level

measurement

over

a wide range of steam density (temperature-pressure

compensation, for steam density).

Westinghouse

identified

inconsistencies

in the guidelines supplied to determine scaling

constants

used to steam density compensate

full-range, upper-range,

and dynamic

head

spans.

At pressures

approaching

2500 psi, the

reactor level indication may be off as

much as

20 percent.

Changes

were

made to the scaling procedure

and plant specific gains

and biases

were determined during system testing.

The inspector

reviewed procedures

1 THP 6030 IMP.315,

1 THP 6030 IMP.316,

2 THP 6030 IMP.415,

and

2 THP 6030 IMP.416, "Reactor Vessel

Level

Indication System

(RVLIS) Train A(B) Calibration (18 Month)," and

determined

the procedures

had incorporated

the correct gain and

bias values

as detailed in RVLIS Scaling

and Calibration Documents

for D.

C.

Cook Units One and

Two (Vendor Information

Control 8P-0986-020-N).

The inspectors verified training was provided to the technicians.

Instrument

and control technicians

were selected

to attend

formal

and on-the-job training (OJT) on RVLIS.

Technicians that were not

trained

on the system did not calibrate

the system

unless

, accompanied

by a qualified technician.

j.

(Closed)

Part

21 Item (315/87001-PP;

316/87001-PP):

Transformer

terminal corrosion that was caused

by acid flux residue left on the.

transformer

leads during the manufacturing process.

The licensee

replaced six (6)

PCB transformers

with qualified dry type transformers

on the 4160V safety related

busses

for each unit.

Unit Two

transformers

were installed

upon receipt from the manufacturer

(Brown Boveri Electric).

No corrosion

was observed.

Unit One

transformers

were placed in a qualified storage'rea'for

approximately

15 months.

During Unit One transformer installation, pitting was

observed

on the plated aluminum terminals.

The licensee notified

the vendor.

The vendor cleaned the transformer leads,

polished the

terminal to remove the pitting, and coated the terminals with

NO-OXIDE grease.

Unit Two transformer terminals were inspected

and

were not pitted.

The vendor indicated that heat from the installed

transformers

caused

the acid flux to subliminate

(change into a gas

and dissipate).

Ten of the transformer terminals

were inspected

by observation

through the louvered panels.

All of the transformers

were in use

at the time.

The terminals

showed

no signs of corrosion

and were

coated with NO-OXIDE grease.

k.

(Closed) Violation (315/85030-01;

316/85030-01):

Failure of the

licensee to take timely corrective action to correct deficiencies

identified in 10 CFR Part 21 reports.

Four items (2.b,d,f,

and

g

of this report) were considered

as

examples for this violation.

AEP procedure

GP 15. 1, "Corrective Action," contained

adequate

steps to prevent the recurrence

of this violation. If the

Corrective/Preventive'actions

cannot

be completed

by the assigned

due date,

extensions

were granted in accordance

with increasing

level of management

approval.

All changes

in report status

or

due dates

were reported to the Trend Coordinator for tracking.

The gA organization

has included

a Part

21 surveillance

in audit

C13-86-31

8 31.1 (Electrical Generation Section)

and in audit

C13-86-21-21.6,

21.8 (Instrument

and Control Section).

No

deficienci es were identi fied.

1.

(Closed) Violation (315/86027-01):

Failure of the licensee

to

adequately

response

time test the Unit One steam generator water

high-high level turbine trip reactor trip.

The licensee

has

adequately

modified procedures

12 THP 4030 STP.205A and 205B,

"Engineered

Safeguards

Features

Time Response

Train A(B)," to

satisfy Unit One

TS 3.3.2. 1 and

TS Table 3.3-5.

m.

(Cl osed)

Open Item (315/86027-02;

316/86027-02):

Change

procedures

1 THP 4030

STP. 100A and

2 THP 4030

STP. 100, "Reactor

Protection

and Engineered

Safeguards

System

Time Response,"

to

measure

the neutron flux signal

time response

from the input of

the first electronic

component in the channel.

The licensee

has

adequately

modified these

procedures

to response

time test the

neutron instrumentation

from the first electronic

component.

Licensee

Event

Re ort (LER

Followu

92700

a.

(Open)

LER (315/87023):

Failure to provide electrical isolation

between

Local Shutdown

and Indication (LSI) panels for Unit One

and Unit Two.

(1)

On November 9, 1987, during an investigation into the

feasibility of using existing Reactor Coolant System

Wide

Range T-Hot and T-Cold indications

(EIIS/AB-TI). for

Regulatory'uide

1.97 compliance,

the licensee

determined that the fuses

(EIIS/FU) required for isolation between the various

LSI panels

(EIIS/PL) were improperly located

on Unit Two and were not

included in the existing design

on Unit One.

Therefore,

a

condition existed that, in 'the event of a fire local to an LSI

panel,

power (both normal

and alternate)

to some or all of the

same unit's remaining

LSI panels

could be lost. 'f power was

lost to all panels,

those indications available locally would

be lost.

In addition, all Wide Range T-Hot and T-Cold

indications,

1 of 4 channels of pressurizer

level indication

(EIIS/AB-LI), and both trains of the Reactor Vessel

Level

Indication System (EIIS/AB-LI) would be lost in the control

room.

According to the licensee's

analysis of this issue, with the

exception of Mide Range T-Hot and T-Cold, all of the process

variables

indicated locally at the LSI panels

would not be

required locally due to their availability in the control

room

and the fact that

a fire at any LSI panel location would not

require

remote

shutdown.

The inspectors,

including

NRC

contractors

(Brookhaven National Laboratory),

performed

a

selected

review of this issue

and concluded that the process

variable indications would still be available in the control

room to enable

a safe

shutdown of the plant.

Each of the units

we'e in a power operation condition

(Mode 1) at the time of

discovery of this issue.

As a result of the identified deficiencies,

the licensee,

on

December

22,

1987,

implemented roving fire watch patrols to tour

the LSI panel

locations within each, unit.

At the request of

Region III personnel,

the licensee,

on December

24, 1987,

upgraded

the roving fire watches to continuous fire watches.

These interim compensatory

measures

were maintained until the

necessary

design

changes

were implemented.

These

changes

were

implemented for Unit Two on December

30,

1987 and for Unit One

on December

29,

1987.

The cause of the electrical isolation deficiencies

was

attributed to an oversight (cognitive personnel

error) by

design engineers

in the design

and engineering

process

associated

with the initial Appendix-R modifications.

The

failure to perform adequate

design

reviews regarding electrical

isolation between

LSI panels is considered

an example of a

potential violation'f 10 CFR 50; Appendix B, Criterion III.

During this inspection,

the inspector

reviewed the

licensee's

implementations of the design

changes

discussed

above.

During this review the inspector determined:

The LSI panels

were located in the following fire zones:

Zone

5

5

33

33

12

12

5

5

34

27

22

24

Power

Feed (Breaker)

20a(Unit 1)

20a(Unit 2)

20a(Unit 2)

20a(Unit 1)

Panel

LSI-3

LSI "4

LSI-1

LSI-5

LSI-2

LSI"6

LSI-3

LSI"4

LSI-1

LSI-5xx

LSI"2

LSI"6xx

Fuse

Addition (Amperes) Unit

10a

5a

5a

10a

10a

sa

5a

10a

The licensee

implemented modification RFC-12-2992 to install

fuses in the LSI panels to provide electrical isolation between

fire zones.

The fuse installation and power feeds to the

panels

are similar for both units.

The LSI panels

located

in Unit l(2) receive their normal

power from Unit l(2).

The

alternate

power source

comes

from Unit 2(l).

Procedure

12

OHP 4023.100.001,

"Emergency

Remote Shutdown," provided

the operator with steps

necessary

to switch from normal to

alternate

power sources.

Power transfer switches

were located

in panels

LSI-4 (supplied power to LSI-3), LSI-5 (supplied

power to LSI-l), and LSI-6 (supplied power to LSI-2).

The

fuses installed were lE qualified.

The design maintained

an

adequate

fuse to fuse amperage

coordination

(2 to 1).

The

inspectors

requested

the coordinating curves for the 10a fuse

to the 20a feeder breaker

on 1/25/88.

The licensee

had not

verified the adequacy of the fuse-breaker

coordination.

The

licensee

informed the inspector

on 1/27/88 that the

10a fuse

to breaker coordination

was not adequate:

This effectively

placed the LSI panels in a similar configuration as initially

identified on ll/9/87.

Failure to apply adequate

design

control measures

for verifying the adequacy of the design

(fuse to breaker coordination) is considered

an example of a

potential Violation of 10 CFR 50, Appendix

B Criterion III.

The licensee

has

conducted training for the Electrical

Generation

Section - Nuclear

(EGS-N)

on properly addressing

Appendix

R requirements

during design reviews.

The operators

were notified of the previously discussed

electrical deficiencies

in Information Review Package

IN-R-0188.

The information adequately

described

the finding, discussed

how

a fire could result in the loss of redundant control

room

indication and described

the corrective actions

(fuse addition).

(4)

The inspectors

evaluated

LER 87023 for meeting the time limit

for reporting as required

by 10 CFR 50.73(d).

The event date

was

November 9,

1987 as stated in the

LER.

The licensee

performed several

evaluations

of this event prior to

determining the event

was reportable

on December

22,

1987.

The report date

was determined to be January

21,

1988.

NUREG-1022,

Supplement

No. 1, (Licensee

Event Report System)

recommends

that the

LER text include

a discussion

on the reason

for having

a significant length of time (>30 days)

between

the event

and reportability date.

The licensee

did not

include this discussion

in LER 87023,

Revision 0.'he

licensee

was notified of this, discontinuity by phone

on

February 3, 1988.

The licensee

committed to submit

a

supplement to the

LER by February

17, 1988,

and to address

the reason

for the delay (>30 days)

between the event

and

reportability date.

This

LER will remain

open pending further

review.

b.

(Closed)

LER (315/87020):

Deficient design which could have caused

insufficient breaker interrupting capability between

Balance of

Plant

(BOP) and Essential

Safety System

(ESS)

250

VDC loads for

Unit One and Unit Two.

On September

17, 1987, during a review of an internal Safety System

Functional

Inspection '(SSFI)

on the auxiliary feedwater

system

(EIIS/BA), it was determined that in the event of a fault in certain

BOP cables

(EIIS/CBL), which would involve distribution panels

from

both independent trains,

a loss of control power on both independent

trains of related

ESS distribution panels

could occur.

The following distribution panels

(EIIS/BL) utilize electrical

circuit breakers

(EIIS/BKR) manufactured

by the Heinemann Electric

Company (Series

0441).

Unit 1:

Train A 1-CCV-CD '-SSV-A1, 1-SSV-A2

Train

B 1-CCV-AB

1-SSV-B

Unit 2:

Train A 2-CCV-CD

Train

B 2-CCV-AB

2-SSV-A1,

2-SSV-A2

2-SSV-B

The breakers

are

used for 250

VDC service.

It was discovered that

the interrupting capability of the Heinemann breakers,

as

used for

D.C.

Cook, is not specified

by the manufacturer at 250

VDC.

Furthermore,

with the specified lower voltage

(125 VDC) interrupting

curves (trip current vs. time),

a comparison of the breakers

with

their upstream

fuses

(Gould-Shawmut Trionic, or Bussman

FRN)

(EIIS/FU) indicated

a lack of coordination for fault currents

above

approximately

1500

amps.

Investigation concluded that this

condition has existed since the initial startup of the units.

10

The design of D.C.

Cook plants

complies with the separation

requirements

of Safety Guide 1. 75 as applied to Class lE

equipment

and circuitry.

The design

and installation criteria

was

implemented

by design specification

DCCEE-627-gCN,

"Electrical Design

and Installation Criteria for Reactor

Protection

and Engineered

Safeguards

Cable Systems."

BOP

cables

may be run in the

same trough with ESS cables provided

the separation criteria for BOP cables

has

been

met.

In this

case,

BOP loads were added to safety-related

DC busses

with an

assumed

adequate

breaker coordination with the 100

amp feeder

fuse.

It was

assumed

that

a

BOP fault would open the breaker

and not the feeder fuse.

Once breaker-fuse

coordination

had been achieved,

a

BOP cable could then be run in conduit or

cable trough with properly coordinated

BOP cables that were fed

from the redundant

DC bus; provided, the

BOP cables

were

no

longer routed in a safeguard

trough.

The licensee

determined that the Heinemann

breakers

could

interrupt

a fault current

up to approximately

1500 amperes.

It

was determined that this fault current protection would begin

at approximately

50 feet of cable length from the breaker.

The

ESS load feeder fuse could have opened

on a fault, given the

wiring fault had occurred within 50 feet of the breaker.

The

licensee

postulated this type of fault as being nonmechanistic

(unlikely to happen)

because

the inadequate

coordination

involved both safety trains.

ESS loads which may have

been

affected were certain containment isolation valves,

reactor

head vent valves, post-accident

sampling valves,

and steam

generator

stop valve

dump valves.

As corrective action,

the licensee

removed all

BOP cables

from

ESS cabinets

SSV-Al and

SSV-B for both units.

The design

added

a 35a lE fuse to lE cabinet

SCP.

The 35a fuse supplies

the

BOP

loads

and the coordination is acceptable

with the 100a

ESS

feeder fuse

(h2 to 1 amperage ratio).

The inspector

found the

installation

was performed adequately

and the correct fuse

.(35a)

was installed.

Even though the licensee identified and corrected this

miscoordination deficiency, this is an additional

example

of failure to apply adequate

design control measures

for

verifying the adequacy of design.

This is considered

an

example

of- a potential violation of 10 CFR 50 Appendix B,

Criterion III.

(2)

Coordination Studies

The licensee

has performed

a Vital AC and

DC bus coordination

study to support Appendix

R requirements.

The inspectors

did

not review these studies.

However, the inspectors

asked the

licensee

to re-examine

the

DC study and determine if the

250

VDC miscoordination

could have

been identified ear lier.

The response

was that the

DC Appendix

R study addressed

fault

currents at the actuated

equipment

end of the cable.

Typical

fault currents

were 149 amperes;

therefore,

the coordination

study appeared

adequate.

The licensee

indicated they were

preparing to re-examine all the vital bus coordination studies.

(3)

Safet

Si nificance

The actual safety significance

appeared

to be small.

For a

safety problem to have existed,

BOP cables

from related panels

would have

had to completely fail and interact simultaneously

with an accident which would have required the affected

ESS

equipment to function.

The

ESS loads that would have

been affected were certain

containment isolation valves,

reactor

head vent valves,

post-accident

sampling valves,

and steam generator

stop valve

(MSIV) dump valves.

All of the valves would have failed to

their safe position (i.e., closed) or would have already

been

closed,

except for the MSIV dump valves.

Each

MSIV has

two redundant

dump valves.

Each valve receives

power from a separate

ESS 250

VDC bus.

The energization

(ESF

Phase

B isolation) of either

dump valve will initiate fast

closure of its associated

MSIV.

The postulated

nonmechanistic

failure of the

DC busses

could prevent the fast closure of the

valves.

However, the MSIVs'ould have

been closed through their

hydraulic closure

mechanism.

Controls for the hydraulic

closures

were located in the control

room and were powered

from the

600

VAC Auxiliary Bus.

The inspector

reviewed the operating procedures

that would be

used to identify and respond to an uncontrolled-depressurization

of all steam generators.

The following procedures

were

reviewed:

1-OHP 4023.001.005

Steam Line Break (1981)

(procedure

superseded

by the following)

1-OHP 4023. E-0

Reactor Trip or Safety Injection (1986)

1-OHP 4023.E-2

Faulted

Steam Generator Isolation (1986)

1-OHP 4023.ECA-2. 1

Uncontrolled Depressurization

of ALL

Steam Generators

(1986)

(procedures

are similar for Unit 2)

12

All of the above procedures

provided instructions to the

operator

on how to identify and respond to MSIVs that failed to

automatically close

on

a Phase

B isolation signal.

It appears

that the licensee

had adequate

procedures

in place to mitigate

the consequences

of a steam line break without fast closure of

the MSIVs.

=-

The inspectors

have

no further concerns

in this area.

C.

(Open)

LER (315/87022):

Potential violation of ESF instrumentation

limiting conditions for operation tolerances

due to Foxboro pressure

transmitter calibration shifts.

These transmitters

were installed

in 1985 for Unit One and

1986 for Unit Two.

Preliminary review of

the last calibrations

determined that there were

24 instances

of

calibration shift on Unit One, with four of these possibly

due to a

calibration error.

Also, two transmitters

were replaced.

Unit Two

experienced

25 instances

of calibration shift with one transmitter

being replaced.

Interviews with instrument

and control technicians

indicated that

Foxboro transmitters typically experience

some calibration shifts

during their first calibration interval

due to the mechanical

zero

and span

mechanism.

Once the transmitters

find a mechanical

equilibrium point (from use),

the technicians

indicated the

transmitters

were stable.

Many of the technicians

had previous experience with existing

Foxboro transmitters.

The new transmitters

work in a similar

manner.

The technicians

gained additional

experience

with the

new transmitters prior to their installation by performing bench

calibrations.

The calibration shift does

not appear to be training

related.

The licensee

committed to submit supplemental

information.

This

will include

a complete analysis of the event

and any corrective

actions to be implemented to reduce the calibration shift.

This

LER will remain

open pending further review.

No other violations or deviations

were identified.

Exit Interviews

The inspectors

met with licensee

representatives

(denoted in Paragraph

1)

on January

28,

1988 to discuss

the scope

and preliminary findings of the

inspection.

A followup meeting

was held with licensee

representatives

(denoted in Paragraph

1) via telecon

on February 3, 1988.

A final

exit meeting

was held with licensee

representatives

(denoted in

Paragraph

1) via telecon

on March 2, 1988.

The licensee

stated that

the likely content of the report would contain

no proprietary information.

13

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