ML17313A534

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Insp Repts 50-528/98-05,50-529/98-05 & 50-530/98-05 on 980531-0711.Violations Noted.Major Areas Inspected: Operations,Maint,Engineering & Plant Support
ML17313A534
Person / Time
Site: Palo Verde  
Issue date: 08/10/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML17313A532 List:
References
50-528-98-05, 50-528-98-5, 50-529-98-05, 50-529-98-5, 50-530-98-05, 50-530-98-5, NUDOCS 9808180187
Download: ML17313A534 (39)


See also: IR 05000528/1998005

Text

ENCLOSURE 2

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket Nos.:

License Nos.:

50-528

50-529

50-530

NPF-41

NPF-51

NPF-74

Report No.:

50-528/98-05

50-529/98-05

50-530/98-05

Licensee:

Facility:

Location:

e

Dates:

Inspectors:

Arizona Public Se'rvice Company

Palo Verde Nuclear Generating Station, Units 1, 2, and 3

5951 S. Wintersburg Road

Tonopah, Arizona

May 31 through July 11, 1998

J. Moorman, III, Senior Resident Inspector

N. Salgado, Resident Inspector

D. Carter, Resident Inspector

V. Gaddy, Resident Inspector

Accompanied By:

M. Kotzalas, Accompanying Inspector

Approved By:

Attachment:

P. Harrell, Chief, Projects Branch D

Supplemental Information

'P808i80187

9808%0

PDR

ADGCK 05000528

6

PDR

I

~,

EXECUTIVE SUMMARY

Palo Verde Nuclear Generating Station, Units 1, 2, and 3

NRC Inspection Report 50-528/98-05; 50-529/98-05; 50-530/98-05

~Oeratione

Effective licensee decision making was demonstrated

by the evaluation performed when

uncertainty was identified in the ability to test trip functions associated

with the four core

protection calculators channels of local power density.

Operations department

performance was good as demonstrated

by use of.three-way communications during

power changes, management oversight and direction, and development of an action

plan to address operability issues (Section 01.1).

The lock was missing on a normally-locked valve in the Unit 1 chemical and volume

control system and was not documented,

as required by procedure.

The failure to

document the removal of a locking device resulted in a loss of configuration control and

is a violation of Technical Specification 6.8.1.a.

This is a repeat violation from a June

1997 inspection (Section 02.1).

proce

Maintenance

Operations personnel conducted effective prejob briefs and demonstrated

good

communication practices during the testing of the Unit 2 steam-driven auxiliary

feedwater pump. Auxiliaryoperators demonstrated

good attention to detail during the

test as demonstrated

by the identification of minor material deficiencies and errors in

dure drawings (Section 04.1).

Knowledgeable technicians used approved procedures to perform routine maintenance

activities. Good work and foreign material control practices were observed

(Section M1.1).

Knowledgeable technicians used approved procedures to conduct surveillance activities

in an acceptable manner (Section M1.2).

Observed material condition of the three units was satisfactory (Section M2.1).

Performance of surveillance tests during the Unit 1 outage was good, as determined by

a review of 20 surveillance test packages.

The tracking of interval-based surveillance

tests effectively scheduled tests, which prevented exceeding the expiration date, as

determined by a review of the surveillance tracking database

(Section M3.1).

Electrical maintenance performed good troubleshooting activities on Startup

Transformer NAN-X02. During the restoration of the startup transformer, good

communications, and management

oversight were noted. Work control tagging was

properly administered throughout all phases of the troubleshooting activities

(Section M4.1).

5

i'

-2-

Encnineerinq

~

Licensee actions to identify deficiencies and initiate corrective actions associated

with a

plant modification, which installed flow meters in the spent fuel pool cooling system were

good. The licensee identified that incorrect material had been used to install the flow

meters; however, the use-as-is evaluation provided appropriate justification based on

testing and material type (Section E2.1).

Plant Su

ort

~

Radiological protection postings of observed radiation, high radiation, and locked high

radiation areas were accurate for existing conditions.

Radiological housekeeping

practices in observed contaminated areas were adequate.

Decontamination

activities'nd

subsequent

surveys of the letdown heat exchanger valve gallery after a letdown line

break in the room were satisfactory

(Section R1.1) ~

~

Good radiological practices were followed during performance of surveillances to

measure chemistry and specific activity of the reactor coolant system.

The chemistry

technician was knowledgeable of the procedures and of the usage of the test

instrumentation (Section R4.1).

t

~

The posting of regulatory notices to workers conformed to 10 CFR 19.11 requirements

and the implementing procedure.

Postings were located in highly-visible and

well-traveled areas (Section R8.1).

l

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't

1

Re ort Details

Summa

of Plant Status

Units 1 and 2 operated at essentially 100 percent power during this inspection period.

Unit 3 began this inspection period at 100 percent power. On July 1, 1998, power was reduced

to approximately 75 percent when the unit entered Technical Specification 3.0.3, after declaring

the local power density channels on all core protection calculators inoperable.

The unit was

returned to 100 percent power on July 2 and remained at that power level for the duration of

this inspection period.

I. 0 erations

01

Conduct of Operations

01.1

Power Reduction After Declarin

AIICore Protection Calculators

CPC

Ino erable

Unit 3

Ins ection Sco

e 71707

On July 1, 1998, the inspectors were notified that Unit 3 entered Technical Specification 3.0.3 when the four local power density (LPD) channels of the CPCs were

declared inoperable.

The inspectors responded to the control room and observed as

operators reduced reactor power. The inspectors observed operator actions, reviewed

unit logs, and licensee notifications of the event.

The inspectors also attended licensee

management

meetings concerning the operability, testing, and recalibration of the

LPD channels.

b.

Observations and Findin s

On June 27, the unit received Plant Protection System B trip and pretrip alarms for

Hl LPD and LO departure from nucleate boiling ratio (DNBR). The licensee declared

CPC B inoperable and bypassed the channel, as allowed by the Technical Specification.

Condition Report/Disposition Request (CRDR) 3-8-0141 and Work Request 945549

were initiated to address the condition. The licensee conducted troubleshooting

activities from June 28 through July 1 on CPC B.

On July 1, the licensee entered Technical Specification 3.0.3 at 11:10 a.m. (MST) after

declaring the LPD trips on all CPCs inoperable.

The licensee reviewed previous

surveillance test Technical Specification for all four LPD channels and determined that

the CPCs were operable.

The licensee believed that the current problem with CPC B

was a testing issue for the late-in-life core conditions and not an operability issue.

Prior to restart from the last refueling outage, the excore neutron detectors were

calibrated such that they would be able to detect the lower leakage from the current

low-leakage core design. To accomplish this, the nuclear detector amplifier gains were

set relatively high by instrumentation and control (l&C) personnel to compensate

for low

core leakage and flux changes.

The l&C technicians performed the adjustment

-2-

Technical Specification in accordance

with Procedure 36ST-9SE03, "Excore Safety

Liner Channel Quarterly Calibration," Revision 11. As the core aged and leakage

increased,

the magnitude of the excore detector signal increased.

On a routine basis,

operators compared the nuclear instrument signal to the secondary calorimetric power

and adjusted the signals as necessary,

using Procedure 40ST-9NI01, "Adjustable

Power Signal Calibrations," Revision 16.

In the CPC, this adjustment is accomplished

by chan'ging the value of an addressable

constant called KCAL. The expected trend

during an operating cycle is for the raw power signal to increase and the value of KCAL

to decrease.

With Unit 3 late in the operating cycle, the signal strength increased and

KCALwas lowered to a point that the potentiometer gains used by l&C personnel for

testing could not add a sufficient signal to generate LPD pretrip and trip signals, as

required by the surveillance test procedure.

At 12:10 p.m., operators commenced the power reduction within the required 1-hour

period allowed by Technical Specification and made the 1-hour emergency notification

to the NRC. The inspectors observed control room operators decrease

reactor power

from approximately 85 to 75 percent in accordance with Procedure 40OP-9ZZ05,

"Power Operations," Revision 20. The operators were given specific instructions as to

the rate of power decrease

and a specific time when the unit was to be in Mode 3 to

meet Technical Specification 3.0.3 requirements.

Operators stabilized reactor power at

approximately 75 percent and verified CPC B would perform its LPD trip function in

accordance with Procedure 77ST-3SB08, "CPC Channel B Functional Test," Revision 7.

The licensee exited Technical Specification 3.0.3 after CPC B and the other three

CPCs were believed to be fullyfunctional. However, CPC B was left in bypass because

the DNBR portion of the surveillance test could not be performed at 75 percent power.

At this reduced power level, the DNBR margin was so high that the DNBR setpoints

could not be tested.

Operators raised reactor power to 86 percent to test the

DNBR portion of the surveillance.

At 6:27 p.m., the licensee declared the LPD and

DNBR trip functions of CPC B operable and removed the channel from bypass.

The

licensee initiated CRDR 3-8-0145 to determine the root cause of the inadequate

surveillance methodology.

During the observed power changes, the control room operators demonstrated

good

three-way communications.

Control room operators plotted the rate of power increase

and closely followed the data to prevent exceeding the limits stated in

Procedure 40OP-9ZZ05.

The shift manager and control room supervisor briefed the

crew several times on the status of the unit and the actions planned.

The shift technical

advisors from the other units assisted the Unit 3 shift technical advisor by performing

routine shift activities, which allowed the Unit 3 shift technical advisor to focus on the

issue of testing and recalibration of the excore detectors.

Licensee managers conducted meetings to discuss the significance of the

CPC channels being considered inoperable and the actions n'ceded to test and return

the CPC channels to operation.

The licensee developed an action plan to address

these issues and discuss the transportability of this problem to the other units. The

licensee concluded that no immediate transportability issue existed for the other units

based on the current gain settings for the excore instrumentation.

f

0

-3-

Conclusions

Effective licensee decision making was demonstrated

by the evaluation performed when

uncertainty was identified in the ability to test trip functions associated with the four core

protection calculators channels of local power density.

Operations department

performance was good as demonstrated

by use of three-way communications during

power changes, management

oversight and direction, and development of an action

plan to address operability issues.

02

Operational Status of Facilities and Equipment

02.1

Failure to Pro erl

Track a Locked Valve Unit 1

Ins ection Sco

e 71707

The inspectors toured portions of rooms containing safety-related equipment in all units

Specification and observed the status of several locked valves.

Observations and Findin s

On June 29, 1998, the inspectors walked down portions of the chemical and volume

control system and identified that Valve CHE-PV-201 Q, letdown backpressure

control,

did not have a secured locking device installed. The inspectors questioned the control

room supervisor as to the status of Valve CHE-PV-201Q and determined that the valve

was isolated and under Active Clearance 98-00464 for mechanical maintenance.

Procedure 40AC-OZZ06, "Locked Val've, Breaker, and Component Control,"

Revision 19, described the controls for valve locking devices.

The position of

components controlled by Procedure 40AC-OZZ06 were tracked in accordance with

Procedure 40DP-9OP19, "Locked Valve, Breaker, and Component Tracking,"

Revision 46. From review of Procedure 40DP-9OP19, Appendix C, "Individual

Valve/Breaker/Component Change Records," located in the control room, the inspectors

determined that Valve CHE-PV-201Q was not being controlled in accordance with this

procedure.

Procedure 40DP-9OP19, Step 3.2, required that the component

description, locked position, position changed to, control room supervisor approval, and

reason for change be entered on an Appendix C tracking sheet.

The licensee stated that, at some point during the maintenance

activity, personnel

removed the valve locking device. After removing the locking device, personnel failed to

make the required entries into the Procedure 40DP-9OP19, Appendix C tracking sheet.

The failure to document the removal of the locking device for Valve CHE-PV-210Q

resulted in a loss of configuration control of the system.

A similar violation was

documented in NRC Inspection Report 50-528;529;530/97-06,

issued June 27, 1997.

The failure to follow Procedure 40DP-90P19 is a violation of Technical Specification 6.8.1 (50-528/9805-01).

l

'

The licensee immediately documented the status of Valve CHE-PV-201Q in

Procedure 40DP-9OP19,

Appendix C, and generated CRDR.1-8-0376 to document this

issue and determine what long-term corrective actions would be implemented.

C.

Conclusions

A lock was missing on a normally locked valve in the Unit 1 chemical.and volume control

system and was not documented,

as required by procedure.

The failure to document

the removal of a locking device resulted in a loss of configuration control and is a

violation of Technical Specification 6.8.1.a.

This is a repeat violation from a June 1997

inspection.

04

Operator Knowledge and Performance

04.1

Steam-Driven Auxilia

Feedwater S stem

AFW Pum

Testin

Unit 2

Ins ection Sco

e 71707

On June 9, 1998, the inspectors observed the licensee perform Procedure 73ST-9AF02,

"AFA-PO1 - Inservice Test," Revision 8.

Observation and Findin s

The inspectors observed control room operators conduct a briefing with personnel

involved with the test. The inspectors verified that maintenance and test equipment

required for the testing was in accordance with the procedure and that calibration

stickers were current.

Control room operators and personnel in the field demonstrated

good three-way communications.

The auxiliary operators (AO) demonstrated

good

attention to details while performing a walkdown of the AFW system, as noted by the

identification of minor packing leakage from Valves AFA-V067 (AFW Pump A discharge

line vent) and SGA-V266 (SG-2 main steam supply to AFW Pump A drain valve). The

leakage did not effect the operability of the system.

The AOs initiated Work

Orders (WO) 944740 and 944765 to have the valves repaired.

The inspectors observed the AOs manually actuate and reset the turbine overspeed trip

device as part of the surveillance.

The AOs identified minor errors in Appendix D

drawings of the surveillance procedure that described the physical layout of the trip

linkage in an untripped condition. The minor errors showed the incorrect position of the

trip valve limitswitches in the reset position. The licensee issued Instruction Change

Request 70536 to correct these discrepancies.

The inspectors also observed maintenance technicians draw an oil sample from the

turbine inboard bearing.

The technicians performed the work activities in accordance

with the work package.

After the AFW pump had operated for 30 minutes, the vibration

technician took the required readings.

On review of the vibration data, the outboard

bearing reading was 0.3289 in/sec, which was in the alert range (>0.325 to

<0.700 in/sec).

Previous vibration readings of this bearing were below the alert range.

-5-

This elevated reading was well within the pump operability limit of 0.700 in/sec.

The

licensee issued CRDR 2-8-0174 to evaluate the elevated reading.

Conclusions

Operations personnel conducted effective prejob briefs and demonstrated

good

communication practices during the testing of the Unit 2 steam-driven auxiliary

feedwater pump. Auxiliaryoperators demonstrated

good attention to detail during the

test as demonstrated

by'the identification of minor material deficiencies and errors in

procedure drawings.

08

Miscellaneous Operations Issues (92901)

08.1

Closed

Violation VIO 50-528 529/9617-01:

Failure.to followprocedures.

In the first example of this violation, operations personnel failed to manually input a

safety equipment status system alarm when a low pressure safety injection pump was

taken out of service.

In the second example, mechanical maintenance

installed a

restraining device on a reactor coolant pump (RCP), which was not described by work

instructions and was not adequately covered under an equipment clearance.

The third

example involved a change in scope to work being performed on a RCP without

submitting the change to a work planner to amend the work instructions.

This violation

resulted from personnel errors.

Licensee corrective action for the first example included coaching of operating crew

supervisors on the procedural requirements for initiating manual safety equipment status

system alarms.

Corrective action for the second and third examples included

counseling

responsible mechanical engineering personnel on the need to fullyevaluate

current plant condition against previous evaluations when determining the actions to be

taken in the field and counseling maintenance

personnel on the need to properly sign

WOs onto the proper clearance.

These corrective actions were adequate to prevent

recurrence.

08.2

Closed

Ins ector Followu

Item

IFI 528/9616-04:

Potential for a nonsafety-related

nuclear cooling water leak into RCP oil collection system.

This item was opened pending a licensee review of a leak in nonsafety-related

nuclear

cooling water piping located near the RCP oil collection system.

The inspectors

expressed

concern that the oil collection tank could fillwith water and go unnoticed and

not provide the necessary capacity for the collection of RCP oil. The licensee initiated

CRDR 9-6;1247 to evaluate the possible methods of water intrusion into the oil

collection tank. The inspectors reviewed the CRDR, the associated

engineering

analysis, and the corrective actions to address the above concerns and found them to

be acceptable.

08.3

Closed

Licensee Event Re ort LER 50-528530/96-004-00:

Reactor trips following a

grid disturbance.

-6-

On August 10, 1996, Units 1 and 3 were operating at 100 percent power when both

reactors tripped on low DNBR following a major electrical grid perturbation.

The reactor

trips resulted from reactor power exceeding the variable over power trip setpoint when

steam bypass control system valves opened in response

to turbine load fluctuations

induced by the grid perturbations.

Required plant equipment and safety systems

responded to the trip as designed.

Allthree units responded similarly to the load

rejection; however, Unit 2 did not trip because the moderator temperature coefficient of

reactivity was less negative than was for Units 1 and 3. The closer the units were to

end-of-core life, the more rapid the power increase and the higher probability of,

reaching variable over power trip setpoint with a decrease

in reactor coolant system

temperature.

The inspectors performed a review of this LER and CRDR 1-6-0160, which documented

the reactor trip investigation.

The reactor trip investigation addressed

the followup

review of plant and system response to the event, including secondary actions to be

completed.

The inspectors considered these actions to be acceptable.

08.4

Closed

IFI 50-530/9802-02:

Assessment

of unplanned loading of the Unit 3 Vital

Battery A.

On January 21, 1998; the AC supply breaker to Vital Battery Charger A opened, leaving

Battery A supplying 125-Vdc Bus PKA-M41 for 35 minutes.

This item was opened to

evaluate the licensee assessment

of how the unplanned loading of the battery affected

battery operation.

The licensee concluded that approximately 100 to 120 amps

discharged, the inadvertent discharge did not affect operability of the battery, and a

battery recharge was not necessary.

The inspectors found no problems with the

licensee's evaluation.

08.5

Lo kee

in

Issues

Units1

2 and 3

On July 10, 1998, a Notice of Violation and Proposed Imposition of Civil Penalty was

issued as a result of the falsification of a surveillance test record (See NRC Investigation

Reports 4-97-022S and 4-1998-014).

The following items are being opened in this

inspection report for administrative purposes to provide tracking numbers for the

violations:

VIO 50-528,529,530/9805-02

Failure to demonstrate operability of offsite

power circuits.

~

VIO 50-528,529,530/9805-03

Required record was not complete and

accurate.

~

VIO 50-528,529,530/9805-04

Failure to submit a LER for a condition

prohibited by Technical Specification.

-7-

II. Maintenance

M1

Conduct of Maintenance

M1.1

General Comments on Maintenance Activities Units 1

2 and 3

a.

Ins ection Sco

e 62707

The inspectors observed all or portions of the following activities performed in

accordance with the following WOs:

835036

"Inspect and Lubricate Valve Stems Valve SIBHV679"

835037

832057

t

788800

"Inspect and Lubricate Valve Stems Valve SIBHV689"

"Calibrate Containment Spray Pump "B" Discharge Flow

Loop 3JSIBFT0348"

"Replace Motor Pinion and Worm Shaft Clutch Gears"

834458

"Perform Inspect/Test iaw 39MT-9ZZ02 of SMB-000H1BC"

b.

Observations and Findin s

The inspectors found the work performed under these activities to be properly

performed.

AIIwork observed was performed with the work package present and in

active use. Work and foreign material exclusion practices observed were good.

Technicians were experienced and knowledgeable of their assigned tasks.

c.

Conclusions

Knowledgeable technicians used approved procedures to perform routine maintenance

activities. Good work and foreign material control practices were observed.

M1.2

General Comments on Surveillance Activities Units 1

2 and 3

a.

Ins ection Sco

e 61726

The inspectors observed all or portions of the following surveillance activities:

'6ST-9SB04

"PPS Functional Test - RPS/ESFAS Logic," Revision 12

73ST-9SI06

"Containment Spray Pumps and Check Valves - Inservice Test,"

Revision 4

(

-8-

73ST-9XI01

"S/8 ¹1 Containment Isolation and Valve Inservice Testing," Revision 15

73ST-9XI09

"Train A LPSI and HP Check Valves - Inservice Test," Revision 3

36ST-9SA01

"ESFAS Train A Subgroup Relay Functional Test," Revision 19

b.

Observations and Findin s

The inspectors found that knowledgeable personnel performed these surveillances

satisfactorily, as specified by applicable procedures.

c.

Conclusions

Knowledgeable technicians used approved procedures to conduct surveillance activities

in an acceptable manner.

M2

Maintenance and Material Condition of Facilities and Equipment

M2.1

Review of Material Condition Durin

Plant Tours

Units 1

2 and 3

a.

Ins ection Sco

e 62707

During this inspection period, routine tours of all units were conducted to evaluate plant

material condition.

b.

Observations and Findin s

On June 18, 1998,

the inspectors observed electrical technicians performing

Procedure 39MT-9ZZ02, "PM/EQPM Inspection of the GL 89-10 Limitorque SMB/SB

Valve Motor Operators," Revision 8, on Valve 3JCTAHV0001 (AFW Pump N suction).

The inspectors noted that the valve switchpack was clean and had no indication of

corrosion.

The inspectors observed the technicians take a sample of the gear box

grease.

The grease was in good condition.

Inspectors'bservation

of plant material condition during this inspection period identified

no major observable material condition deficiencies.

Minor deficiencies brought to the

attention of the licensee were documented with work requests.

Conclusions

Observable material condition of the three units was satisfactory.

0

M3

Maintenance Procedures and Documentation

M3.1

Outa

e Surveillances

Unit 1

Ins ection Sco

e 61726

Inspectors evaluated the system used to track interval-based surveillance requirements

and reviewed 20 surveillance test packages and the associated WOs for surveillances

completed during the Unit 1 seventh refueling outage.

The inspectors evaluated the

following surveillance test packages:

36ST-9SE02

"Excore Linear Monthly Calibration," Revision 10

32ST-9ZZ74

"Molded Case Circuit Breaker Surveillance Test," Revision 13

40ST-9SF01

"CEA Operability Checks," Revision 0

77ST-9SB06

"CEAC 2 Calibration," Revision 10

73 ST-9ZZ21

73 ST-9ZZ21

"Snubber Visual Examination," Revision 4

"Snubber Visual Examination," Revision 5

73ST-9XI28

"Containment Isolation Check Valves-Inservice Test," Revision 2

73ST-9XI18

"Diesel Generator 'B'ir Receiver Inlet Check Valves-Inservice Test,"

Revision 2

73ST-9XI02

"SG N2 Containment Isolation Valves-Inservice Test," Revision 14

32ST-9ZZ02

"18-Month Containment Penetration Conductor Low Voltage Overcurrent

Protection (SST)," Revision 4

32MT-9PE01

"18-Month Cleaning, Inspection, and Testing of the Class 1E Diesel

Generator," Revision

1

73ST-9HP03

"Hydrogen Monitoring Subsystem Leakage Monitoring," Revision

1

40ST-9AF06

"AuxiliaryFeedwater Pump AFN-P01 Monthly Valve Alignment,"

Revision 2

40ST-9HF01

"ESF Pump Room Air Exhaust Cleanup System Operability Test 4.7.8a,"

Revision 4

40ST-9ZZ01

"Locked Valve Monthly Surveillance," Revision 4

32ST-9PK03

"18-Month Surveillance Test of Station Batteries," Revision 14

- IO-

. 41ST-1ZZ04

"Weekly Shutdown Electrical Distribution Checks," Revision 13

36ST-9RC01

"Pressure Instrumentation Calibration," Revision 3

73ST-1DG01

"Class 1E Diesel Generator and Integrated Safeguards

Surveillance

Test-Train A," Revision 9

73ST-1DG02

"Class 1E Diesel Generator and Integrated Safeguards

Surveillance

Test - Train B," Revision 9

b.

Observations and Findin s

The inspectors evaluated STAT, the database

used to track interval-based surveillance

requirements.

The licensee maintained the database

by inputting test data on a daily

basis.

The date, time, and whether the test satisfied the requirements was manually

'ntered

into STAT. This information was double checked upon receipt of the hard copy

of the work package.

The licensee used STAT to generate reports that listed tests that

exceeded the scheduled date or were past 100 percent of the allowed time interval.

This system effectively alerted the licensee to surveillance intervals approaching

expiration.

The licensee used the STAT database

to generate a generic list of outage surveillances.

Necessary signatures of operations personnel were obtained prior to commencement of

the surveillances and all data met acceptance

criteria. The inspectors determined, from

interviews with 18 C technicians, that they were knowledgeable of the surveillance

procedures and use of the measuring and test equipment.

c.

Conclusions

Performance of surveillance tests during the Unit 1 outage was good, as determined by

a review of 20 completed surveillance test packages.

The tracking. of interval-based

surveillance tests effectively scheduled tests, which prevented exceeding the expiration

date, as determined by a review of the surveillance tracking database.

M4

Maintenance Staff Knowledge and Performance

M4.1

Troubleshootin

Activities on Startu

Transformer NAN-X02 Unit 1

a.

Ins ection Sco

e 62707

On June 3, 1998, inspectors observed electrical technicians perform troubleshooting

activities on Startup Transformer NAN-X02. The transformer gas detector had

experienced spurious alarms.

The inspectors reviewed WO 837480, the

troubleshooting action plan, and active clearances.

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1

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Observations and Findin s

The technicians followed the troubleshooting instructions and documented the findings,

as required.

Proper occupational safety and health administration practices for high

elevations were used while working'on top of the transformer.

The system engineer,

technicians, and operators demonstrated

good communication practices, such as repeat

backS.

The inspectors verified work control tags were properly installed on all electrical

sources to the transformer and that all electrical phases were properly grounded.

During troubleshooting activities, no other work was allowed to be conducted within the

switchyard and testing of the emergency diesel generators and gas turbine generators

was suspended.

Troubleshooting activities did not identify a single problem attributed to the gas detector

alarms; however, several loose mechanical connections were discovered and corrected.

Since Startup Transformer NAN-X02was placed back into service, no further alarms

have occurred.

On completion of the troubleshooting activities, the inspectors observed the removal of

grounding straps from the transformer.

The Unit 1 Shift Manager monitored the removal

of the grounding straps and movement of a bucketed crane within the switchyard.

Operations conducted a briefing prior to the transformer work emphasizing caution

during this high risk evolution in the switchyard. Operations oversight of this evolution

was good. The inspectors also observed the AOs remove the clearance and rack-in five

13.8-kV breakers in accordance

with Procedure 41OP-1AN01, "13.8 KV Electrical

System (NA)," Revision 23.

Conclusions

Electrical maintenance performed good troubleshooting activities on Startup

Transformer NAN-X02. During the restoration of the startup transformer, good

communications and management

oversight were noted. Work control tagging was

properly administered throughout all phases of the troubleshooting activities.

III. En ineerin

E2

Engineering Support of Facilities and Equipment

E2.1

S ent Fuel Pool Coolin

S stem Modification Evaluations

Units 1 2 and 3

Ins ection Sco

e 37551

The inspectors reviewed the circumstances

of a nonconformance condition that existed

in the spent fuel pool cooling system in all three units (Trains A and B) except Unit 1

Train B. The inspectors reviewed associated WOs, evaluations, and held discussions

with design engineering personnel.

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b.

Observations and Findin s

The modification provided for the installation of an Annubar-style flow meter in the

PC system discharge piping. During the final review of the implementation plant change

work orders (PCWO), the licensee identified a problem with the installation of the

modifications. The design modification specified piping material classification HCCA,

which required the use of ASME,Section II, Class 3 material. The implementing PCWO

specified commercial-grade material. The modification included installation of a 1-inch

stainless steel, socket-welded piping cap.

However, the PCWOs specified American

Society for Testing and Materials commercial-grade material for this component.

The inspectors reviewed the deficiency work order that provided a conditional release

disposition to leave the pipe cap, as installed, and rework with the correct material at a

later date.

The licensee based the use-as-is conditional release on the following:

The pipe caps were the same material (A182/SA182 Type-304 stainless steel)

specified for the application; therefore, the material was compatible for the

system pressure ratings and allowable stress.

The pipe caps were installed and welded by certified welding personnel using

qualified w'eld procedures.

I

The welding process required liquid penetrant examinations of the final weld

passes.

These nondestructive examination tests'were satisfactorily completed.

The modification successfully passed the inservice leak test.

Visual examinations were successful.

Maintenance engineering recommended replacement of the pipe caps with the correct

grade of material during the next 12-week schedule.

The inspectors verified'that the

licensee initiated deficiency work requests to rework the pipe caps on all affected trains.

The licensee initiated CRDR 9-8-0998 to evaluate how the wrong material was

translated from the design modification into the individual PCWOs.

Review of the

licensee's evaluation willbe tracked as an IFI (50-528,529,539/9805-05).

Conclusions

Licensee actions to identify deficiencies and initiate corrective actions associated

with a

plant modification, which installed flow meters in the spent fuel pool cooling system were

good. The licensee identified that incorrect material had been used to install the flow

meters; however, the use-as-is evaluation provided appropriate justification based on

testing and material type.

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IV. Plant Su

ort

Radiological Protection and Chemistry Controls

General Comments on Radiation Protection

RP

Controls

Units 1

2 and 3

Ins ection Sco

e 71750

The inspectors toured the radiological controlled area of all units and observed RP

postings of radiation, high radiation, locked high radiation, and contaminated areas.

Observations and Findin s

On June 29, 1998, the inspectors observed numerous contaminated areas where loose

materials (e.g., station pole, lead shielding, floor drain cover, rags, and poly bags) were

left unattended.

These deficiencies were brought to the attention of RP management

and were quickly corrected.

Upon exiting the radiological controlled area, an inspector alarmed the personnel

contamination monitor. While performing a required postcontamination monitor frisk, a

discrete particle was detected on the front of the inspector's clothing. The RP technician

performed a detailed survey and decontaminated

the inspector's clothing with adhesive

tape.

The particle had an activity of 6,000 dpm. The RP technician appropriately

questioned the inspector as to the locations that had been entered.

The inspector

stated that he had not entered any contaminated areas.

RP technicians conducted surveys of the areas the inspector had traveled.

An

additional particIe with an activity of 10,000 dpm was found while performing large area

wipe-downs in the letdown heat exchanger valve gallery, outside a posted contamination

area.

This area had been sprayed with reactor coolant from a recent letdown line break

that occurred on May 24. The majority of the valve gallery was subsequently

decontaminated

and released.

The inspectors reviewed licensee contamination surveys

of the letdown heat exchanger valve gallery after the letdown line break and found them

to be acceptable.

The licensee reposted the letdown heat exchanger valve gallery as a

contaminated area pending further decontamination.

On June 30, the inspectors conducted a tour of the Unit 3 auxiliary and radwaste

buildings with a member of RP management.

The inspectors and the licensee identified

several contamination control devices (drip basins) that may not have performed their

intended function of containing minor valve stem leakage and boron crystals.

The

licensee also found a drip basin device that was mounted to a remote valve actuator,

which had been operated and caused the drip basin to turn upside down. The inspector

noted that the basin did not affect the operability of the valve. The licensee performed a

survey of the area and found no contamination and corrected the placement of the drip

basin.

RP management

directed the RP decontamination crew to evaluate the

condition of all basins in each unit. The decontamination crew inspected all basins and

corrected the small number of basins found to be inadequate

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Allobserved radiation areas, high radiation areas, locked high radiation areas, and

contaminated areas were adequately posted with signs appropriate for existing

conditions.

c.

Conclusions

Radiological protection postings of observed radiation, high radiation, and locked high

radiation areas were accurate for existing conditions.

Radiological housekeeping

practices in observed contaminated areas were adequate.

Decontamination activities

and subsequent

surveys of the letdown heat exchanger valve gallery after a letdown line

break in the room were satisfactory.

R4

Staff Knowledge and Performance

R4.1

Chemist

Sam

lin of the Reactor Coolant S stem

RCS

Unit 3

a.

Ins ection Sco

e 71750

Inspectors observed the performance of two surveillance tests associated

with the

chemistry and specific activity of the RCS. The following procedures were used during

performance of the surveillances and were reviewed by inspectors:

74ST-9RC01

"Reactor Coolant System Chemistry Surveillance Test," Revision 5

74ST-9RC02

74OP-9SS01

"Reactor Coolant System Specific ActivitySurveillance Test," Revision 6

"Primary Sampling Instructions," Revision 12

74CH-9XC80 "Basic Chemistry Analysis," Revision 0

74CH-9ZZ72

"Operation and Calibration of the lon Chromatograph," Revision 9

74CH-9XC40 "Operation and Calibration of the Hewlett-Packard Gas Chromatograph,"

Revision 4

74CH-9ZZ06

"Boron Autotitrator Operation and Calibration," Revision 19

74CH-9XC50 "Operation and Calibration of the Gamma Spectrometry System,"

Revision 7

74CH-9ZZ15

"RCS Gross ActivityDetermination," Revision

1

74CH-9ZZ87

"Iodine-131 Dose Equivalent Determination," Revision 5

74CH-9XC58 "Data Correlation, Evaluation and Review," Revision 4

74DP-OCH02

"LAC Performance," Revision 2

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74DP-9CY04

"Systems Chemistry Specifications," Revision 4

b.

Observations and Findin s

The inspectors observed the performance of the surveillance tests for measuring the

amount of dissolved oxygen, chlorides, fluorides, and specific activity of the RCS and

~

noted that all of the surveillance requirements were met. The chemistry technician

complied with the applicable procedures and followed good radiological practices.

These practices included keeping the tygon tube, used for RCS flow to the sampling

sink, in the sink drain when not in use; rinsing the sink with demineralized water after

preparing the RCS sample; and implementing an effective system of glove layering to

maintain noncontaminated

hands.

In addition, the chemistry technician was

knowledgeable of the procedures and usage of the test instrumentation.

c.

Conclusions

Good radiological practices were followed during performance of surveillances to

measure the chemistry and specific activity of the reactor coolant system.

The

chemistry technician was knowledgeable of the procedures and of the usage of the test

instrumentation.

R8

Miscellaneous RP &Chemistry Issues

R8.1

Postin

of Notices to Workers

Units 1

2 and 3

. a.

Ins ection Sco

e 71750

I

The inspectors verified the licensee's posting of notices to workers, as required by

10 CFR 19.11 and Procedure 93DP-OLC05, "Regulatory Interaction and

Correspondence

Control," Revision 1.

b.

Observations and Findin s

Five bulletin boards containing the required information were located in conspicuous

areas throughout the site. This included the entrance to the protected area, bottom

floors of Buildings A and B, pedestrian exit of the parking lot in front of Building E, and

pedestrian exit to the parking lot in front of the warehouse.

Conclusions

The posting of regulatory notices to workers conformed to 10 CFR 19.11 requirements

and the implementing procedure.

Postings were located in-highly-visible and

well-traveled areas.

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E.

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V. Mana ement Meetin s

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management at

the conclusion of the inspection on July 15, 1998. The licensee acknowledged the

findings presented.

The inspectors asked the licensee whether any material examined during the inspection

should be considered proprietary.

No proprietary information was identified.

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i

ATTACHMENT

PARTIALLIST OF PERSONS CONTACTED

Licensee

D. Carnes, Unit 1 Department Leader, Operations

D. Fan, Acting Department Leader, System Engineering

R. Fullmer, Director, Nuclear Assurance

R. Henry, Site Representative,

Salt River Project

W. Ide, Vice President, Nuclear Engineering

D. Kanitz, Engineer, Nuclear Regulatory Affairs

A. Krainik, Department Leader, Nuclear Regulatory Affairs

J. Levine, Senior Vice President, Nuclear

D. Mauldin, Director, Maintenance

D. Marks, Section Leader, Nuclear Regulatory Affairs

G. Overbeck, Vice President, Nuclear Production

F. Riedel, Department Leader, Operations Standards

J. Scott, Director, Site Chemistry

M. Shea, Director, Radiation Protection

D. Smith, Director, Operations

B. Thiele, Section Leader, Reactor Engineering

T. Trieckef, Department Leader, Outage and Planning

e

IP 37551

IP 61726:

IP 62707:

IP 71707:

IP 71750:

IP 92901:

INSPECTION PROCEDURES USED

Onsite Engineering

Surveillance Observations

Maintenance Observations

Plant Operations

Plant Support Activities

Plant Operations Followup

ITEMS OPENED, CLOSED, AND DISCUSSED

~Oened

50-528/9805-01

VIO

Failure to document valve configuration change.

50-528,529,530/9805-02

VIO

Failure to demonstrate operability of offsite power circuits.

50-528,529,530/9805-03

VIO

Required record was not complete and accurate.

50-528,529,530/9805-04

50-528,529,530/9805-05

VIO

Failure to submit an LER for a condition prohibited by

Technical Specification.

IFI

DM Piping Material Information incorrectly translated into

PCWOs.

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Closed

50-528,529/9617-01

50-528/9616-04

VIO

Failure to followprocedures by operators with three

different examples.

IFI

Potential for a nonsafety-related

NCW leak into RCP oil

collection system.

50-528,530/96-004-00

50-530/9802-02

LER

Reactor trips due to grid disturbance

IFI

Assessment

of unplanned loading of Unit 3 Vital Battery A.

LIST OF ACRONYMS USED

AFW

AO

CFR

CPC

CRDR

LPD

MST

NRC

SFP

PCWO

RCP

RCS

PDR

RP

VIO

WO

auxiliary feedwater

auxiliary operator

Code of Federal Regulations

core protection calculator

condition report/disposition request

departure from nucleate boiling

disintegrations per minute

instrumentation and control

inspector followup item

licensee event report

local power density

mountain standard time

Nuclear Regulatory Commission

spent fuel pool

plant change work order

reactor coolant pump

reactor coolant system

public document room

radiation protection

violation

work order