ML17311A674

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Insp Repts 50-528/94-37,50-529/94-37 & 50-530/94-37 on 941201-950114.No Violations Noted.Major Areas Inspected: Plant Status,Onsite Response to Events,Operational Safety Verification,Maint & Surveillance Operations
ML17311A674
Person / Time
Site: Palo Verde  Arizona Public Service icon.png
Issue date: 02/22/1995
From: Wong H
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML17311A673 List:
References
50-528-94-37, 50-529-94-37, 50-530-94-37, NUDOCS 9503010293
Download: ML17311A674 (44)


See also: IR 05000528/1994037

Text

0

APPENDIX A

U.S.

NUCLEAR REGULATORY COMMISSION

REGION IV

Inspection

Report:

50-528/94-37

50-529/94-37

50-530/94-37

Licenses:

NPF-41

NPF-51

NPF-74

Licensee:

Arizona Public Service

Company

P.O.

Box 53999

Phoenix,

Arizona

Facility Name:

Palo Verde Nuclear Generating Station,

Units 1,

2,

and

3

Inspection At:

Maricopa County, Arizona

Inspection

Conducted:

December

1,

1994,

through January

14,

1995

Inspectors:

K. Johnston

H.

Freeman

J.

Kramer

A. MacDougall

D. Garcia

Senior Resident

Inspector

Resident

Inspector

Resident

Inspector

Resident

Inspector

Resident

Inspector

South

Texas Project

Approved:

ng,

C

>e

,

eacto

roJects

Branc

~ z~/~s-

ate

Ins ection

Summar

Areas

Ins ected

Units

1

2

and

3

Routine,

announced

inspection of plant

status,

onsite

response

to events,

operational

safety verification,

maintenance

and surveillance

observations,

operations

and engineering

followup, and licensee

event report

(LER) review.

Results

Units

1

2

and

3

0 erations

Inspectors

continued to note

improvements

in the conduct of operations

in all

three units.

For example,

an attentive auxiliary operator identified

a small

crack on

an emergency diesel

generator

(EDG) intake manifold and the licensee

appropriately

performed

an operability evaluation of the manifold leak and

concluded that the diesel

was operable

(Section 2.4)..

Operations

personnel

also responded

promptly,to

a leaking pressurizer

spray valve (Section 2.6).

However,

a minor weakness

was noted in that Unit 3 operators failed to

9503010293

950224

PDR

ADOCK 05000528

6

PDR

1

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independently verify the position of the essential

chiller disconnects

as

required

by procedure

(Section 2.3).

Maintenance

Overall, inspectors

noted

improvements

in maintenance activities which appear

to reflect management

attention to work in the field and to plant material

condition.

For example:

~

A test of 'the essential

ventilation system,

to develop filter

replacement criteria in support of the licensee's

implementation of the

revised maintenance

rule, identified

a low flow condition that would not

have

been identified otherwise

(Section 2.2).

The good maintenance

practices

and supervision

were observed

during the troubleshooting,

repair,

and testing of an atmospheric

dump valve (Section 3.3

and 4).

The licensee

has noticeably

improved the material condition of the

EDGs, but longstanding deficiencies

in the nonsafety-related

diesel trip system contributed to extended unavailability

(Section 3.2).

Continued minor weaknesses

in the area of work instruction quality and

procedural

adherence

were noted

by the inspectors.

In one instance,

an

unnecessary

instruction to check for hydrogen

gas

when breaching the charging

system

was ignored

by the maintenance

personnel.

This demonstrated

the lack

of a thorough work package

review by both the maintenance

team leader

and

maintenance

worker (Section 3. I).

En ineerin

Engineering followup of some issues

was very thorough,

although

some

NRC

prompting was required to assure

timely resolution.

Examples of thorough

engineering

followup included the review of a misassembled

snubber in Unit 3

to assure this was

an isolated deficiency (Section

6)

and the review of NRC

Information Notice (IN) 94-60 regarding

power limits with inoperable

main

steam safety valves which identified

a weakness

in their accident

analyses

as

well as

a potentially generic issue

(Section

5. 1).

However, the timeliness of

the accident

analyses

review was left as

an unresolved

item, pending further

review.

Engineering troubleshooting

on the Unit 3 turbine-driven auxiliary feedwater

pump

(TDAFWP) was not well controlled.

The success

of the troubleshooting

effort was largely attributed to the direct involvement of senior engineering

management.

While this demonstrated

an appropriate

level of work oversight,

it highlighted

a weakness

in engineering

troubleshooting

processes

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Summar

of Ins ection Findin s:

~

One inspection followup item was noted in Section 3.2.

~

One unresolved

item was identified concerning

the licensee's

evaluation

of NRC Information Notice 94-60 addressing

power operation with main

steam safety valves

gagged

(Section

5. 1).

Violation 530/9416-04,

concerning

the bent

EDG connecting rod,

and

Violation 529/9420-05,

concerning

the failure to follow procedures

for a

10 CFR 50.59 evaluation,

wer e closed

(Section 7).

LER 528/94-07,

Revision 0,

was closed

(Section 8).

LERs 528/94-08,

Revision 0, 529/94-03,

Revision 0,

and 529/94-04,

Revision 0, were

closed

(Section 9).

Attachments:

~

Attachment

1 - Persons

Contacted

and Exit Meeting

~

Attachment

2 - List of Acronyms

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DETAILS

1

PLANT STATUS

1.1

Unit

1

Unit

1 began the inspection period in Hode

1 at approximately

18 percent

power.

The unit had completed repairs to

a leaking pressurizer

vent valve at

the end of the previous inspection period

and was conducting

power ascension

to full power.

On December

2,

1994,

the unit reached

98 percent.

On December

14, there

was

a major grid disturbance

in central California.

At

approximately

1:30 a.m.,

the grid frequency lowered to around

59 hertz

and

resulted

in load swings of a maximum of 100 megawatts for about

7 minutes.

During the event,

control

systems

responded

as designed,

no equipment

damage

occurred,

and

no other operator actions

were required.

On December

19, the licensee

implemented

a Technical Specification

(TS)

change,

which raised the

maximum allowed power from 98.2 percent to 100

percent with one main steam safety relief valve inoperable

in each generator,

and then raised

power to 100 percent.

The unit remained at essentially

100 percent

power until commencing

a downpower

on January

14 for steam

generator

(SG) chemistry hideout return.

The unit ended the inspection period

at

70 percent.

Power was increased

to 100 percent the following day.

1.2

Unit 2

Unit 2 operated

throughout the inspection period at essentially

100 percent

power.

On December

10,

a partial loss of control

room annunciators

occurred

when

a power supply to the annunciator

system failed.

The annunciators

were

restored within 15 minutes

(Section 2.1).

The California grid disturbance

affected Unit 2 as in Unit 1.

1.3

Unit 3

Unit 3 began the inspection period in Hode

5 for a

SG tube inspection.

On

December

17, the unit entered

Hode 2,

and

began

power ascension

to 100 percent

power.

The unit remained

at essentially

100 percent

power through the

remainder of this inspection period.

2

OPERATIONAL SAFETY VERIFICATION

(71707)

2. 1

Partial

Loss of Control

Room Annunciators

Unit 2

On December

10,

1994, at about 9:46 a.m., technicians

were performing

corrective maintenance

in one of the power supply cabinets for the control

room annunciator

system in Unit 2.

While removing

a circuit card,

one of the

technicians

dropped

a flat washer into

a power supply inverter.

This caused

the failure of the inverter

and blew the fuse for the inverter backup

power

supply.

i

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When the fault occurred,

control

room operators

received

an annunciator

power

supply trouble alarm and several

alarm conditions:

emergency

safeguards

features

(ESF) equipment

and chemical

and volume control

system

equipment

alarm windows;

SG and feedwater

systems

alarm windows were in fast flash;

and

turbine generator,

auxiliary systems,

and the turbine trip first out had all

alarm windows out.

These

alarms

would not respond to any control

board

push

buttons

and were considered

inoperable.

About one-half of the control

room alarm panels

were available to the

operators;

and the plant monitoring system,

safety equipment status

system,

emergency

response

data acquisition

system,

and quality safety parameter

display system were operable.

The operators

implemented the "Loss of

Annunciators"

abnormal

procedure

and reviewed the plant TS, event reporting

manual,

and emergency

plan

and determined that

no event classification

was

required.

At about

10:08 a.m., technicians

replaced

the blown fuse

and

restored

the control

room annunciator

system.

The inspector

reviewed applicable

procedures

and determined that the operators

"appropriately followed plant procedures

and that safety-related

equipment

remained

operable.

The inspector also met with the maintenance

engineer

and

determined that the system

responded

as expected

when the inverter

and backup

power supply fuse failed.

The maintenance

engineer initiated

a condition

report/disposition

request

(CRDR) which included

a corrective action to

install

a guard

around the inverters to minimize the potential for similar

events.

The inspector

concluded that these

actions

were appropriate.

2.2

ESF Switch ear

Room Essential

Ventilation Air Handlin

Unit Testin

Unit

1

On January

6,

1994, during testing,

the licensee

found that the

ESF switchgear

room essential

Air Handling Unit (AHU), HJA-Z03,

was not supplying the design

air flow of 4100 standard

cubic feet per minute to the 4160 volt safety-

related switchgear

rooms.

The system engineer

had developed

a special test to

determine

the differential pressure

across

the intake filter that would

prevent the

AHU (HJA-Z03) from supplying the design basis air flow.

This

information would then

be used

as the basis for periodically replacing the

filters.

When the engineers

started

the test the indicated flow was only 2900

standard

cubic feet per minute without any obstruction

across

the intake

filter.

The shift supervisor

immediately declared

the

AHU inoperable.

'Although the

AHU is not specifically included in the plant TSs, it was required to be

operable to support operability of the Train A 4160 volt safety-related

load

center.

The licensee's

administrative controls required the

AHU to be

returned to an operable

status within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or the affected

4160 volt load

center

be declared

inoperable.

The inspector

reviewed the licensee's

procedures

and

TSs

and concluded that the licensee

appropriately controlled

operability of the

AHU.

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The licensee

conducted

a detailed

walkdown of the ventilation lineup and found

the return supply damper for the

AHU only 10 percent

open

(normal position is

100 percent

open).

Technicians

found that

a nut had

come loose

and allowed

the damper to close to the

10 percent

open position.

The damper

was

repositioned,

the air flow retested,

and the

AHU was declared

operable.

The

site shift manager verified that the supply damper for the Unit

1 Train

8

ESF

switchgear

room essential

AHU and both trains of the Unit 2 and

3

ESF

switchgear

room essential

AHUs were in the

100 percent

open position.

The licensee initiated

a root cause of failure CRDR.

The inspector

concluded

that the licensee

appropriately restored operability of the

ESF switchgear

room essential

AHUs and corrected

the immediate safety concern.

The inspector

will review the licensee's

investigation of this event during

a future

inspection.

2.3

Inde endent Verification Unit 3

During

a review of the essential

chill water system

on January

13,

1995, the

inspector

noted that the licensee failed to perform the independent

verification of the essential

chiller disconnects

as required

by procedure.

The inspector notified the shift supervisor of the problem.

The shift

supervisor dispatched

an operator to verify that the disconnects

were closed.

Subsequent

review identified that

an open disconnect situation would have

been

alarmed in the control

room.

There were

no such alarms at the time.

The licensee

performed sections of Procedure

430P-3ECOl/2,

"Essential

Chilled

Water Train A/B," for the chemistry department

to draw

a weekly sample of the

circulating water system.

The procedure,

in part, required the operators

to

open the disconnects,

start the circulating water

pump, close the disconnects,

and independently verify the disconnects

were closed.

The inspector

noted in

a review of procedure

records that

on two occasions,

Unit 3 operators

had

failed to perform the independent verification.

The licensee

performed several

corrective actions.

The shift supervisor

directed

an operator

to check the disconnect positions.

They were in the

appropriate positions.

The licensee

issued

a night order to the operations

personnel

emphasizing

the requirement to perform independent verifications.

In addition, the licensee initiated

a

CRDR to evaluate

the problem.

The inspector

concluded that the licensee

performed

adequate

corrective

actions.

The inspector

noted that the operators

would receive several

control

room alarms if the disconnects

were left open.

The lack of alarms

provided

the operators

an indication that the disconnects

were closed although

an

independent verification was not performed.

Therefore,

the inspector

concluded that the failure to follow procedure

was of minor significance.

The inspector

noted that

a recent trend analysis

performed

by Nuclear

Assurance identified that instances

of equipment

and valve misalignments

were

substantially greater

in Unit 3 than the other two units.

In response

to

these findings, Unit 3 operations

management

was taking action to improve

performance.

The example

noted in this section

would tend to support the

performance

trend identified by Nuclear Assurance.

2.4

EDG Intake Manifold Leak

Unit I

While performing

a routine surveillance test

(ST)

on

EDG IA on December

27,

1994,

an auxiliary operator

noted what appeared

to be

a cracked weld on the

number four right cylinder intake manifold.

The hairline crack was

approximately 3/4 inches

long that ran across

the weld at the flange.

The

crack was apparently

"through-wall" which caused

a barely detectable air leak

while the

EDG was operating.

The licensee

conducted

an operability evaluation

and concluded that the crack did not affect the operability of the

EDG.

On December

28, the inspector

observed

the cracked weld.

The inspector noted

that the crack was across

the weld.

This weld joined the cylinder head

bolting flange to

a square

section of pipe (approximately

6 x 6 inches)

which

provided forced air from the intake plenum.

The inspector

noted that the weld

appeared

to be old,

due to some oxidation indications in and around the weld.

The inspector concluded that the crack did not appear to be propagating

and

did not appear to affect the structural integrity of the manifold.

The inspector

reviewed the licensee's

operability determination.

The

inspector

noted that the licensee's

inspection of the crack included

a

certified level III visual weld inspector.

The level III inspector,

and

engineering

and maintenance

personnel

concluded that the crack was

insignificant.

The licensee

also concluded that if the weld failed

circumferentially 360 degrees

around the pipe (unlikely due to crack

orientation),

the other nine intake flange welds were sufficient to support

the intake plenum and that the

EDG would remain operable.

The inspector

concluded that the licensee

took the appropriate

steps to ensure

that the deficiency did not affect the operability of the

EDG.

The inspector

agreed with the licensee's

conclusion that the crack was insignificant and did

not affect the operability of the

EDG.

Finally, the inspector concluded that

the auxiliary operator

had done

an excellent job in identifying and notifying

manag'ement

of the presence

of the crack.

2.5

EDG Material Condition - Units I

2 and

3

Throughout the inspection period, the inspectors

noted improving material

conditions of the

EDGs in all three units.

The inspectors

noted that, in some

cases,

all of the standing oil and the oil absorbent

devices

had

been

removed.

In previous inspections,

inspectors

had noted

numerous oil leaks

and

30 or

more different oil absorbent

devices

saturated

with oil on one diesel

alone.

At the exit meeting,

the Director of Maintenance

mentioned that they had

targeted

the deficiencies of the diesels

and that they would continue to

improve the material conditions.

The inspectors

concluded that the licensee

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was making good progress

in correcting minor deficiencies,

such

as oil and

cooling water leaks,

in an effort to improve the material conditions of the

EDGs.

2,6

Pressurizer

S ra

Valve Leaka

e - Unit 2

On December

21,

1994, operations

determined that

one of two pressurizer

spray

valves in Unit 2 had developed

a

6 gallon per minute packing leak.

Operators

entered

the containment

and isolated the spray valve which stopped

the leak.

Repairs

were planned for the Unit 2 refueling outage

scheduled

to begin

February 4,

1995.

Operations

demonstrated

prompt response

to the leakage

indication.

3

MAINTENANCE OBSERVATIONS

(62703)

3, 1

Char in

Pum

Packin

Re lacement - Unit 2

On January

5,

1995,

the inspector

observed

mechanical

maintenance

technicians

install

new packing

on the plungers of charging

Pump

A in Unit 2.

The work

was being performed using model work Procedure

31NT-9CH01,

"Charging

Pump

Disassembly

and Assembly."

The inspector

observed

good radiological

protection work practices

by the mechanics

and good oversight of the activity

by an

RP technician.

The inspector

noted that the model work instructions

were detailed

and technically accurate.

The inspector

noted that the procedure

had

a step to perform

a hydrogen

gas

check when the system

was breached if directed

by the team leader.

The

inspector determined'hat

the lead mechanic

had not received instructions

from

the team leader concerning the hydrogen

check

and subsequently

did not perform

the check when the system

was breached.

In discussions,

the team leader

stated that

he reviewed the work order,

but did not notice the step to perform

the hydrogen

gas check.

The inspector

noted that the licensee

did not historically have

any problems

with excessive

hydrogen

gas in the charging

system

and that the failure to

perform the step

had low safety significance.

However, the inspector

was

concerned

that the team leader

and the lead mechanic did not thoroughly review

the work procedure.

The inspector discussed

the problem with the mechanical

maintenance

department

leader

who agreed that the prejob briefing did not meet management's

expectations.

The licensee's

corrective actions

included reinforcing the need

to conduct thorough prejob briefings especially

when the team members

had not

recently worked

on

a particular system.

The licensee

also decided that the

step to perform the leak check was not necessary

and

removed the step from the

procedure.

The inspector

concluded that the licensee's

response

was

appropriate.

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3.2

Multi le

EDG Tri

s

Unit 2

On December

14,

1994, the Unit 2

EDG

B was started

in the emergency

mode

and

satisfactorily loaded for a monthly ST.

After the

EDG was unloaded for the

engine

cooldown,

the surveillance

procedure

required that the emergency

mode

interlock defeat

switch

be placed in the off position which enabled

the test

mode trip circuitry.

When the operator

moved the switch to the off position,

the incomplete

sequence

alarm momentarily

came in and the

EDG tripped.

Operators

declared

the

EDG inoperable

and the maintenance

engineers

developed

a troubleshooting

plan.

The inspector

observed electrical

maintenance

engineering

troubleshoot

the

test

mode circuitry.

The engineers

suspected

that

some relays must have

opened

long enough to cause

the trip solenoid to deenergize.

The technicians

removed the most probable relays

and found two normally energized

relays with

open contacts that would not pick up.

On December

15, after replacing the faulty relays,

operators

started

the

EDG

in the test

mode to perform

a maintenance

run.

During the test run, the

EDG

tripped during the cooldown cycle

on

an indicated high jacket water

temperature

alarm.

The technicians

suspected

the problem was in the

nonsafety-related

pneumatic trip circuitry.

The technicians

found air leaks

in the check valve associated

with the high jacket water temperature

alarm

and

the temperature trip valve.

These

components

were replaced

and the

EDG was

again started

in the test

mode

and immediately tripped

on incomplete

sequence

since it did not reach rated

speed.

The technicians

found

some minor air

leaks

and

a leaking check valve that was replaced.

On December

16, the

EDG was successfully started

in the test

mode.

During the

cooldown cycle, the

EDG tripped

on

an indicated

low turbocharger

lube oil

pressure

alarm.

The technicians

found

a piece of debris in the check valve

associated

with the low turbocharger

lube oil pressure

alarm.

The debris

damaged

the seat of the check valve

and caused it to leak.

The technicians

replaced

the check valve and successfully

started

the

EDG in the test

mode.

The

EDG would not stop after completion of the cooldown cycle

and would not

shutdown

when the emergency

pushbutton

was depressed.

The

EDG was stopped

by

manually tripping the fuel racks.

The licensee

suspected

the problem with the

EDG not stopping

was caused

by

sluggish operation of the pneumatic control valves.

Two control valves were

replaced

and the

EDG was successfully started

and shutdown in the test

mode.

During the evening of December

16, the

ST was satisfactorily completed

and the

EDG was restored

to an operable

status.

The inspector reviewed the troubleshooting

work orders,

the

EDG logs,

the

control

room logs,

and discussed

with the system engineer

the root cause of

failure analysis.

Based

on this review, the inspector

had the following

observations:

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All five of the problems

would not have prevented

the

EDG from starting

and

running in the emergency

mode.

However, the

EDG was unavailable

(would not

start

on

an emergency signal) for a total of 20 hours2.314815e-4 days <br />0.00556 hours <br />3.306878e-5 weeks <br />7.61e-6 months <br /> during the

troubleshooting activities.

The inspector

was concerned that having the

EDG unavailable for this period of time increased

the vulnerability of the

plant.

~

Engineering

had previously developed

an action plan to reduce the number of

EDG test

mode trips.

The corrective actions

included replacing

continuously energized

Agastat relays every

10 years

and replacing the

check valves with an improved check valve that had better seating

characteristics

and

an internal filter.

These

improvements

were scheduled

for installation during the Unit 2 refueling outage in February

1995.

~

The licensee's

performance. during the troubleshooting efforts may have

been

inconsistent.

The inspector

observed

good troubleshooting

and work

practices

during the first problem with the relays.

However,

one of the

leaking checks

valves

may have

been

caused

by debris introduced into the

air system during replacement

of an earlier check valve.

Additionally, the

cause of one event

was not fully corrected

and

may have subsequently

caused

the problem with not being able to stop the

EDG.

~

The performance of the 8-hour surveillance

requirement to check the offsite

power sources

with an inoperable

EOG were not consistently

documented

in

the unit log.

However, the procedure

used to perform the

ST was correctly

completed

every

8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />

as required

by the plant TS.

The licensee

issued

a

night order emphasizing

management's

expectation that compliance with TS

action statements

be documented

in the unit log.

The inspector

concluded

that these

actions

were appropriate.

At the

same time the inspector

was raising questions

regarding the cool-down

cycle trips, the licensee

was also reviewing these

events.

The licensee

initiated

a root cause of failure

CRDR for the multiple failures.

The

Director of Engineering

also raised the priority of the effort to reduce the

number of test

mode

EOG trips to level

1 action plan (highest priority) to

include the experience

of the

EDGs in all three units.

The inspector will

review the licensee's

formal root cause

evaluation

and corrective actions

during

a future inspection

(Followup Item 529/9437-01).

3.3

Atmos heric

Dum

Valve

ADV

Maintenance

Unit 3

During routine

ST of the ADV-185 in Unit 3, technicians

noticed that the valve

was making

a "popping" noise in the closed direction.

The licensee

suspected

that the noise

was coming from the valve actuator

and rebuilt the valve

operator.

During the retest,

the valve continued to make the popping noise

'and its stroke time placed it in the enhanced

monitoring range.

The licensee

then suspected

a problem internal to the valve and disassembled

the valve on

t

December

15.

On December

19, the valve was reassembled

and successfully

retested.

0

'I

1

-11-

The inspector

reviewed the vendor technical

manual

(VTH) and model work

Procedure

31HT-9SG04,

"ADV Disassembly

and Assembly."

The inspector

noted

that all the critical acceptance

criteria in the

VTH were included in the

procedure.

The inspector

noted that the model

procedure

used

a different type

and arrangement

of packing rings than described

in the

VTH.

The system

engineer

stated that engineering

had done

an evaluation to include the

ADVs in

the licensee's

valve packing program.

The inspector

noted that the work order

had

a step to repack the valve per the valve .packing installation procedure

and referenced

the engineering

evaluation.

The inspector

concluded that

engineering

had

a good basis for using

a different packing arrangement

and

that the model work instructions

were thorough

and technically accurate.

The inspector

observed

mechanical

maintenance

personnel

disassemble

the valve

on December

15.

The inspector noted

good supervision

in the field and good

work practices

by the mechanics.

The maintenance

engineer

conducted

a

detailed review of the parts

and thought that the valve piston

may have

been

periodically hanging

up on the piston rings.

The piston rings were slightly

worn at the split which caused

increased friction at the location of the ring

split.

The engineer

suspected

that the piston ring wear resulted

when the

valve was stroked several

times during the testing in November

1994.

Testing

is typically performed with an upstream isolation valve closed,

isolating

steam which acts to lubricate the ri,ngs.

The mechanical

maintenance

engineer initiated

a

CRDR to document the root

cause of failure.

As

a corrective action, the engineers

were considering

putting

a caution in the procedure for adjusting the valve positioner that

would require water to be injected into the valve bonnet in cases

of multiple

strokes without steam.

The inspector

concluded that the licensee's initial

corrective actions

were appropriate.

3.4

Other Haintenance

Observed

~

Haintenance

of medium voltage circuit breakers

Type AH-4.16-250

Unit

1

~

Electrical design

change

on the 4. 16

kV bus breakers - Unit

1

~

New fuel receipt - Unit 2

~

Installation of new

AC input supply circuit breaker for the "D" battery

charger - Unit 2

4

SURVEILLANCE OBSERVATIONS

(61726)

ADV Testin

Unit 3

On December

19,

1994, the inspector

observed

a 100 percent stroke test of an

ADV from the control

room.

The licensee

performed

ST 43ST-3SG04,

"Testing

ADV's in Node 1," Section 8.7.

The inspector

observed

good

command

and

control of the evolution by the control

room staff.

The inspector

noted

good

f

I

1

j

f

-12-

communications

between

the control

room operators

and the operators

at the

ADV.

The inspector

noted the coordination

between

the control

room operators

minimized plant perturbations

during the stroke test.

The test

was conducted

successfully.

The inspector

concluded operations

exhibited

a strong

performance

throughout the test.

5

ONSITE ENGINEERING

(37551)

5.1

NRC IN 94-60:

Power

0 eration with Main Steam Safet

Valves

HSSV

~Ga

ed

The inspector

conducted

a review to determine if the licensee

had evaluated

NRC IN 94-60, "Potential Overpressurization

of Main Steam System,"

issued

on

August 22,

1994.

IN 94-60 discussed

a potential for overpressurizing

the main

steam

system during previously evaluated

accident

scenarios

when

one or more

HSSV was inoperable.

The inspector selected this IN to review because

Unit

1

was operating at 98 percent

power in compliance with TS due to having two

inoperable

HSSVs.

The

IN discussed

that most plant

TS allow power operation with inoperable

MSSVs at

a power level that was equivalent to the capacity of the remaining

HSSVs.

The basis of this

TS assumes

that the maximum allowable initial power

level is

a linear function of HSSV capacity.

However,

Westinghouse

determined

that the linear assumption for reducing

power levels with inoperable

HSSVs

was

nonconservative

and

may result in overpressurizing

the secondary

system during

accident

scenarios

with inoperable

MSSVs.

The licensee's

operational

experience

review

(OER) group screened

the

IN as

applicable

in September

1994 since the basis for the

TS for power operation

with inoperable

HSSVs also

assumed

a linear reduction of power with HSSV

capacity.

The inspector

noted that the licensee

conducted

a preliminary

review of the condition addressed

in the

IN in October

1994.

The licensee

noted that the original safety evaluations of the loss of condenser

vacuum

(LOCV) accident concurrent with a total loss of feedwater

were performed with

all the

HSSVs operable

and did consider the potential of overpressurizing

the

secondary

system

when operating at the reduced

power levels with inoperable

MSSVs.

The safety analysis

engineers

used the previously licensed

Combustion

Engineering

(CE) simulation of the

LOCV accident

and ran the program with up

to two inoperable

MSSVs in each

SG and determined that there

was

no

significant increase

in main steam pressures

with inoperable

HSSVs.

The

licensee

believed the condition in Unit

1 with two inoperable

HSSVs

was

acceptable

based

on this initial review.

The

OER group scheduled

a detailed

review of the

IN to be completed

by March 31,

1995.

The inspector

noted that the licensee

had submitted

a TS amendment

to allow

Unit

1 to operate

at

100 percent

power with the two inoperable

HSSVs.

The

inspector questioned

the licensee's

decision to not complete

a detailed,

formal evaluation of the concerns

in the

IN prior to completing the

TS

0

)

)

,

-13-

amendment.

Based

on the inspector's

concerns,

the

OER group moved

up the

review date for the

IN to December

31,

1994.

On December

14, the

TS amendment

for raising power to

100 percent

was issued

by the Nuclear Reactor Regulation

and Unit

1 returned to 100 percent.

In December

1994, after Unit

1 had increased

power to 100 percent,

safety

analysis

engineers

determined that although the previous

LOCV analysis

assumed

initial plant conditions

and parameters

that would generate

the most limiting

primary pressure,

these conditions did not assure

maximum secondary

pressure.

Additionally, the engineers

determined that

CE had not previously formally

evaluated

the'secondary

overpressurization

condition discussed

in the IN.

As a result,

the safety analysis

group changed

the initial plant conditions

and parameters

used in the

LOCV accident to increase

the heat transfer to the

SGs

and

make the secondary

side pressure

more limiting.

The analysis

was

performed for the condition in Unit

1 with two inoperable

MSSVs

and

was found

to be acceptable.

However, preliminary runs were performed for additional

inoperable

HSSVs

and the potential for overpressurizing

the main steam

system

may occur at lower power levels with the maximum of four HSSVs in each

SG

inoperable

(as allowed by TS).

The inspector

reviewed the

IN and

had numerous

discussion

with the safety

analysis

engineers,

licensing engineers,

and the

OER group.

Based

on these

discussions

the inspector concluded that the licensee

had conducted

an

appropriate initial review of the concerns

addressed

in the IN.

Additionally,

the inspector

agreed with the licensee that operation in Unit

1 at

100 percent

power with two inoperable

HSSVs was not

a safety concern.

However, the

inspector

was concerned that the licensee

had not identified the incorrect

assumptions

with the

LOCV accident during the development of the

TS submittal

for returning to 100 percent

power with two inoperable

HSSVs.

The licensee initiated

a

CRDR to perform the detailed analysis of the

condition

and determine if any changes

to the

TS for inoperable

HSSVs

was

required.

The inspector will review the

CRDR during

a future inspection to

determine if the licensee

should

have discovered

the incorrect assumptions

in

the

LOCV accident simulation during the development of the

TS amendment

submittal

and confirm whether

a generic safety concern exists for secondary

overpressurization

events

(Unresolved

Item 528/9437-02).

5.2

TDAFWP Failure

Unit 3

On December

20,

1994, the inspector

observed

licensee

personnel

perform

portions of the work activity associated

with the investigation of an

overspeed trip of the Unit 3 TDAFWP.

On December

19, operators

noted low

TDAFWP steam supply line temperatures

and started

the

pump to raise the

temperature

in the line.

This action was taken in response

to the licensee's

analysis of previous

TDAFWP trips caused

by condensation

which had formed in

cold steam

supply lines.

In accordance

with operating

procedures,

operators

started

the

TDAFWP by opening valves in one

steam supply.

The

pump started

as

!

I

I

l

~

'I

1

~

~

designed,

and operators

opened

valves in the second

steam supply line.

The

TDAFWP began to overspeed,

and subsequently

tripped.

Operators

declared

the

TDAFWP inoperable,

the unit entered

a 72-hour

TS action

statement,

and

a

CRDR was initiated.

An investigation

team assembled

to

determine the root cause of the

TDAFWP trip.

The team

was led by system

engineering

personnel.

On December

20, the inspector

observed

the team

members

as they participated in collecting

and verifying data

and facts.

The inspector

observed

good communication techniques

between the different

organizations.

The investigation

team developed

an action plan to recreate

the scenario of

December

19.

The steam piping low points were purged of condensation,

and

initial testing revealed that previous condensation

buildup in the horizontal

section just upstream of a check Valve (SG-V43) upstream of the steam supply

line header

was the cause for the turbine to trip on overspeed.

However, the

performance of the governor valve remained

in question

and the team determined

that further testing in the presence

of a representative

from the governor

valve vendor was warranted.

On December

21, another action plan was developed

to start the

TDAFWP in the

same valve configuration with established

atmospheric

conditions.

Test

instrumentation

and strip chart recorders

were installed to record the turbine

responses.

An initial run of the

TDAFWP was aborted

due to an instrument fitting leak.

The horizontal section

upstream of the check Valve (SG-V43)

had higher steam

line temperatures

and, therefore,

the decision

was to remove

some of the

insulation to allow the piping to cool

down.

The inspector

noted that the Director of System Engineering

and

a system

engineering

team leader

were present

during this testing

and was involved in

ensuring that questions

regarding

personnel

overtime limits, approved

work

orders for removing the insulation,

and action plans for testing the

TDAFWP

were properly addressed.

The system engineering

team leader discussed

his hand written instructions for

resuming the test with the relief test coordinator

who had been involved with

the earlier testing.

A prejob briefing was held in the control

room with all

the personnel

involved in the testing of the

TDAFWP.

The prejob briefing was

presented

by the Director of System Engineering

using the handwritten

instructions to discuss

the evolutions that were going to take place.

While the inspector

found that the involvement of the director of site

engineering

indicated appropriate

management

attention to this testing,

the

inspector

observed that considerable direct involvement appeared

necessary

to

ensure that the troubleshooting effort was conducted properly.

The inspector

noted that the action plan lacked prerequisites,

precautions,

limitations,

and

contingency plans to insure that issues

such

as temperature

changes,

communications

between organizations,

and shift turnover were adequately

I

I

f

0

-15-

addressed.

In addition,

the licensee

did not have instructions to provide

documentation of test parameters

or results.

The inspector discussed

these findings with the

Director of System

Engineering

who concurred that the testing

was not conducted

consistent

with

his expectations.

The

Director concluded that

a special test procedure

was

not appropriate for this test.

While the inspector

agreed that this testing

did not require the rigor of a special test procedure,

the testing involved

several disciplines,

extended

through shifts,

and involved configuration

control

issues

which warrant sufficient formality to assure effective

communication of the testing process.

A CRDR was initiated by site

engineering to review guidance for engineering

troubleshooting.

The inspector

will review the guidance

in a future inspection.

6

FOLLOWUP - HAINTENANCE

(92902)

Misassembled

Hechanical

Snubber

Unit 3

In July 1994,

an

NRC inspector questioned

the performance of a mechanical

snubber installed

on

a Unit 3 auxiliary feedwater

pump steam trap line after

he found the snubber

would not rotate

on its pins.

Although an engineer

initially confirmed that the snubber

would not rotate,

during

a subsequent

inspection,

the snubber

was found to rotate

as expected.

On December

14,

1994, with Unit 3 transitioning from Mode

5 to Mode 4,

a

licensee

engineer

performed

a followup inspection

and noted that the cold

position of the snubber

was the

same

as the hot position

he had previously

observed.

The licensee

subsequently

discovered that the snubber

had

been

inappropriately

reworked

and misassembled.

The snubber,

which was

supposed

to

be

a 1/4 thousand-inch-pound

(kip) snubber,

had

been

assembled

with both 1/4

kip and 1/2 kip snubber parts.

The net result

was that the snubber

had

a

shorter stroke than design.

The licensee

replaced

the snubber.

The licensee

determined,

based

on documentation of testing during the

1992

Unit 3 refueling outage,

that this snubber

had

been intact when it was removed

from the system

and

had

been tested satisfactorily.

However,

a comparison of

the as-found

and as-left pin-to-pin dimensions

indicated that the reinstalled

snubber did not match the snubber

which had

been

removed.

This indicated that

the snubber

had

been modified after testing

and prior to reinstallation.

There

was

no documentation of a modification to the snubber

and the licensee

stated that it was not their practice to rework small

snubbers.

The inspector

determined that the snubber deficiency could not have

been

readily identified with the plant in Mode

1 and that the licensee's initial

review in response

to the July 1994 inspection finding has

been reasonable.

The inspector questioned

whether the licensee

had assurance

that this was

an

isolated

case.

The licensee

performed

walkdowns of a large

sample of 1/4 kip

snubbers

and performed

a complete review of test documentation.

They

~

~

0

-16-

concluded that this had

been

an isolated

case.

The inspector

reviewed the

licensee's

efforts

and found them to be appropriate.

The licensee

subsequently

interviewed maintenance

personnel

involved in the

removal

and testing of the snubber in the

1992 refueling outage.

However,

personnel

involved in the outage

could not recall

a modification having

been

performed

and reiterated

the practice of discarding

1/4 and 1/2 kip snubbers

with deficiencies.

The licensee

was not able to contact

some contract

maintenance

workers which are

no longer working for the licensee.

The

inspector determined that the licensee

had performed

a reasonable

investigation of this matter.

The inspector questioned

whether

an evaluation

should

be performed to

determine the impact of the as-found condition of this snubber

on system

performance

during

a design

basis

event.

The snubber,

which was in its fully

extended position when installed with the steam line cold, would not have

allowed pipe movement

as the system

heated

up.

The licensee

evaluated

the

configuration

and found that the loading

on the line would not have

exceeded

the design basis.

The inspector

noted that the line was relatively long and

small in diameter,

providing considerable flexibility, which supports

the

licensee's

analysis.

Although the licensee

could not identify how the snubber

was misassembled,

corrective action

was taken to inform craft involved in snubber testing of the

misassembled

snubber

and to reiterate

the expectation that snubbers

of this

size are not to be reworked.

The inspector

found this action to be

appropriate.

7

FOLLOWUP - ENGINEERING

(92903)

7. 1

Closed

Violation 530 9416-04:

Bent

EDG Connectin

Rod - Unit 3

This violation was issued for failure to promptly identify and correct

a bent

connecting

rod in Cylinder 6-L of Unit 3

EDG

B which occurred during

a rocker

arm failure on July 28,

1993.

The licensee

noted

symptoms of the bent

connecting

rod on October 20,

1993,

but failed to identify the problem until

Harch 23,

1994.

The inspector reviewed the licensee's

investigation

and corrective actions

regarding the violation.

The licensee

concluded that the violation was caused

by failing to promptly validate assumptions

used in analyzing the indications

obtained

on October 20,

1993,

and

compounded

by poor communications

between

and within organizations.

Additionally, the licensee

concluded:

~

Some of management's

expectations

were not clearly communicated (i.e., to

challenge

assumptions

and follow issues to closure),

l

e

-17-

~

Communications

problems existed within and

between organizational

departments

leading to poor interaction or coordination of evaluation

findings,

~

Issues

were not followed to closure in a timely manner,

and

~

A self-critical attitude did not exist at all levels which led to

a less

aggressive

approach

to the problem.

The inspector

noted that the licensee's

findings of the root cause of the

violation were very similar to the

NRC findings related to this event

documented

in

NRC Special

Inspection 50-530/94-16.

The inspector

reviewed the licensee's

corrective actions of which the most

significant action involved the licensee's

reengineered

organization

which was

implemented

in August 1994.

Two of the contributing factors to the violation

were poor communications

and

a lack of management

involvement.

The

reengineer ed organization

now consists of teams for each

system that include

engineering,

maintenance,

and planning personnel.

The closer working

relationship

was intended to foster freer communications,

especially

between

the maintenance

engineers

and the maintenance craft.

NRC Inspection

Report

50-530/94-16

noted that the maintenance craft and planner suggested

to remove

the crank case

inspection

cover in December

1993,

but did not pursue

the

suggestion.

Additionally, the licensee

has

implemented

a daily meeting

between

department

leaders

and other senior managers

to discuss

plant status,

emerging issues,

daily maintenance

plans,

and other issues.

Engineering

issues/concerns

are

specifically addressed

once per week at these

meetings.

Also, important

issues that are identified by the licensee's

condition reporting

system

are

discussed

at the daily meeting.

By effectively using this meeting,

important

issues

can

be identified, prioritized and tracked

by senior management.

The

inspector

noted

improved communications

and more management

involvement since

implementation of the reengineered

organization.

Another change that was not specifically implemented

in response

to the

violation was the operability determination

Procedure

(40DP-90P26).

The

inspector

reviewed the procedure

and noted that it stated that,

"whenever the

ability of a structure,

system or component

(SSC) to perform its specified

function is called into question

by an indication of a potential deficiency

. then the operability of the

SSC shall

be determined

.

.

. Otherwise,

the

SSC should

be declared

inoperable."

In this case,

the licensee

concluded that

the

EDG was operable;

however,

the system engineer

was concerned

about the

long term reliability caused

by a potential deficiency.

The operability

procedure

would require deliberate

and timely actions to resolve the

engineer's

concern.

Finally,

NRC Inspection

Report 50-530/94-16

noted that the retest,

following

the rocker

arm rework in July 1993, consisted

only of a simple surveillance

I

l

-18-

run and failed to identify the degraded

condition caused

by the bent

connecting

rod.

The licensee

decided that to ensure that pertinent data

are

available for EDG operability determinations

following extensive

rework, that

a leak-down check

and

an engine analysis

would be required.

The inspector

reviewed the licensee's

postmaintenance

retest

development

procedure

and

verified that the procedure

required the inclusion of the specified tests.

The inspector

concluded that the actions

taken

by the licensee

were

appropriate.

7.2

Closed

Violation 50-529 9420-05:

Failure to Follow Procedures

for a

10 CFR 50.59 Evaluation

This violation involved the failure to follow procedures

when

a 10 CFR 50.59

screening

identified that TSs were affected

by

a design

change.

In this

instance,

the design

change

was

implemented

before

a

TS change

was submitted

and approved

by the

NRC.

The design

change

rerouted

the location of the

condenser

vacuum exhaust

and the affected

TS depicted the location of the

condenser

vacuum exhaust.

As corrective action, licensee

management clarified expectations

regarding

changes

to Tss

and the need for timeliness

in processing

change requests.

Also,

on November 2,

1994, the licensee

submitted

a

TS amendment

request

which

depicted the

new location for the condenser

vacuum exhaust.

The inspector concluded that the actions

taken

by the licensee

were

appropriate.

7.3

En ineerin

Res

onse to Overs

eed of Turbine-Driven

Pum

s Caused

b

Governor Valve Stem Bindin

NRC IN 94-66 documented

recent

problems regarding binding of governor valves

for turbine-driven

pumps that have resulted in overspeed trips.

On December

21,

1994, the inspector

reviewed internal licensee

memorandum

addressing

this

issue for all three units.

The inspector interviewed the system engineer

and

determined that the licensee

has taken appropriate

action to address

the

concern.

The inspector

was concerned with the recent

overspeed trip of the Unit 3

TDAFWP that occurred

on December

19 (Section 5.2).

The investigation

determined that the overspeed trip did not occur

as

a result of governor valve

stem binding.

As part of the investigation,

the linkage to the governor valve

had

been disconnected

from the servo motor and determined to have full freedom

of motion.

In addition, the vendor representative

inspected

the components

and found no discrepancies.

The governor valve stem

had just been replaced

in

the Unit 3

TDAFWP during the previous outage.

The inspector

noted that the licensee's

investigation to determine

whether

stem binding was occurring

was thorough

and exhaustive.

,~ l

.e

-19-

8

ONSITE REVIEW OF

LER

(92700)

Closed

LER 528 94-07

Revision 0:

Missed Surveillance

Re uirement for

Containment

Pur

e Isolation Valves

This

LER was submitted

when the licensee identified that the thermal

overload

protection circuits had never

been verified to be bypassed

continuously or

under accident conditions per

TS Surveillance

Requirement 4.8.4.2. 1.

Two

containment

purge isolation valves

each isolate the intake

and the exhaust

lines for the containment

purge system.

The licensee

had discovered this

omission

on November

3,

1994, during

a design basis validation review.

The inspector

reviewed the actuation signals to these four isolation valves.

The inspector

noted that the valves receive

a containment isolation actuation

signal

and

a containment

purge isolation actuation

signal

(CPIAS).

The

licensee's

design

basis

review had revealed that the 18-month

ST that

had been

performed for Surveillance

Requirement 4.8.4.2.

1 had ensured that the thermal

overloads

were bypassed for a containment isolation actuation signal,

but had

not ensured this feature for a CPIAS (a different section of the

same

circuit).

The inspector

reviewed the Updated, Final Safety Analysis Report for the

consequences

of the containment

purge isolation valves not being operable.

The containment

purge

system

was designed to operate

only while shutdown,

and

the

CPIAS was intended to terminate the purge which would substantially

reduce

potential offsite radiological

exposures

in the event of a fuel handling

accident

in containment.

However, the radiological

consequences

of a fuel

handling accident

have

been calculated without assuming

CPIAS operation,

and

the offsite doses

are still a small fraction of 10 CFR Part 100 limits.

Therefore,

the inspector

concluded that the licensee's

failure to test the

thermal

overload

bypass feature for the

CPIAS was of low safety significance.

The inspector

reviewed the licensee's

corrective actions.

The inspector

noted

that the licensee

intended to include steps

in an operations

procedure to

ensure that the thermal

overload

was bypassed

during

a CPIAS.

The licensee

concluded that this would meet the once per 18-month requirement.

The

inspector

concluded that the intended corrective actions

were appropriate.

9

IN OFFICE REVIEW OF

LERS

(90712)

The following LER was closed following an in-office review in accordance

with

inspection

module 90712:

~

LER 528/94-08,

Revision 0,

TS Required

Shutdown to Repair Leaking

Pressurizer

Vent Path Valves.

4

-20-

~

LER 529/94-03,

Revision 0, Missed

TS

LCO Action for Monitoring Reactor

Coolant System

Boron Concentration

~

LER 529/94-04,

Revision 0, Class

lE Batteries

in a Degraded

Condition

10 DISPOSITIONED

LAMP COVERS

ON REMOTE SHUTDOWN PANEL

Inspection

Report 528/94-34 identified that the inspector

found lamp covers

mispositioned

on the remote

shutdown

panel

in Unit 2.

As

a corrective action,

the licensee initially considered

installing security card reading

doors at

the entry of the remote

shutdown panels in all units.

Subsequently,

the

licensee

revised their planned preventive actions.

They preliminarily propose

to install plexiglass

covers

over the panels with some type of securing tag.

The inspector

found this planned action to be acceptable.

I

1

t

ATTACHMENT I

I

PERSONS

CONTACTED

1. I

Licensee

Personnel

J. Bailey, Vice President,

Nuclear Engineering

& Projects

P. Crawley, Director, Nuclear

Fuel

J.

Dennis,

Section

Leader,

Operations

Support

A. Fakhar,

Hanager,

Site Hechanical

Engineering

B. Grabo,

Section

Leader Compliance,

Nuclear Regulatory Affairs

A. Krainik, Hanager,

Nuclear Regulatory Affairs

D. Hauldin, Director, Site Haintenance

and Hodifications

J. Scott, Director, Chemistry

H. Sharp,

Instructor, Operations Training

W. Stewart,

Executive Vice President

R. Stroud,

Regulatory Consultant,

NRA

1.2

NRC Personnel

K. Johnston,

Senior Resident

Inspector

H. Freeman,

Resident

Inspector

J.

Kramer,

Resident

Inspector

A. HacDougall,

Resident

Inspector

B. Olson, Project Inspector

t

1.3

Others

J. Draper, Site Representative,

Southern California Edison

R. Henry, Site Representative,

Salt River Project

F.

Gowers, Site Representative,

El

Paso Electric

All personnel

listed above attended

the Exit meeting held

on January

18,

1995.

2

EXIT MEETING

An exit meeting

was conducted

on January

18,

1995.

During this meeting,

the

inspectors

reviewed the scope

and findings of the report.

The licensee

did

not express

a position

on the inspection findings documented

in this report.

The licensee

did not identify as proprietary

any information provided to, or

reviewed

by the inspectors.

~ l

(

)

i

'i

ADV

AKU

CFR

CPIAS

CRDR

EDG

ESF

IN

kip

LER

LOCV

HSSV

NRR

OER

SG

.SSC

ST

TDAFWP

TS

VTN

ATTACHNENT 2

ACRONYNS

atmospheric

dump valve

air handling unit

Code of Federal

Regulation

containment

purge isolation actuation

signal

condition report/disposition

request

emergency diesel

generator

emergency

safeguards

features

Information Notice

thousand

inch pound

licensee

event report

loss of condenser

vacuum

main steam safety valve

Nuclear Reactor Regulation

operating

experience

review

steam generator

structure,

system or component

surveillance test

turbine-driven auxiliary feedwater

pump

Technical Specification

vendor technical

manual

I

1

~ 4

0

I