ML17310B478

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Insp Repts 50-528/94-20,50-529/94-20 & 50-530/94-20 on 940508-0611.Violations Noted.Major Areas Inspected:Plant Status,Onsite Response to Events,Operational Safety Verification,Maintenance & Surveillance Observations
ML17310B478
Person / Time
Site: Palo Verde  Arizona Public Service icon.png
Issue date: 07/12/1994
From: Wong H
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML17310B475 List:
References
50-528-94-20, 50-529-94-20, 50-530-94-20, NUDOCS 9408020062
Download: ML17310B478 (52)


See also: IR 05000528/1994020

Text

APPENDIX B

U.S.

NUCLEAR REGULATORY COMMISSION

REGION IV

Inspection

Report:

50-528/94-20

50-529/94-20

50-530/94-20

Licenses:

NPF-41

NPF-51

NPF-74

Licensee:

Arizona Public Service

Company

P.O.

Box 53999

Phoenix,

Arizona

Facility Name:

Palo Verde Nuclear Generating-Station,

Units 1, 2,

and

3

Inspection At:

Haricopa County, Arizona

Inspection

Conducted:

Hay 8 through June ll, 1994

Inspectors:

K. Johnston,

Senior Resident

Inspector

H. Freeman,

Resident

Inspector

.

J.

Kramer, Resident

Inspector

A. HacDougall,

Resident

Inspector

Accompanying Personnel:

B. Holian,

NRR Project

Manager

J. Ganiere,

NRR Intern

Approved:

ong,

se

,

actor

roJe

s

rane

7

g +/gl

ate

Ins ection

Summar

Areas

Ins ected:

Routine,

announced

inspection of plant status,

onsite

response

to events,

operational

safety verification, maintenance

and

surveillance observations,

and refueling activities.

Results

Units

1

2

and

3

211

Control

room communication

weaknesses

were determined

to be

a significant

contributing factor in a Unit 2 reactor trip (Section 2.3)

and

a Unit 3

turbine-driven auxiliary feedwater

pump overspeed trip (Section

5. 1).

In the

case of the overspeed trip, these

communications

weaknesses

resulted

in a

failure to follow procedures

which was determined to be

a violation.

94080200b2

940729

PDR

  • DOCK 050D0528

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Plant operators

failed to adequately 'consider the impact

on the operability of

a Unit 2 emergency

diesel

generator

(EDG) after racking

a breaker out for an

automatically actuated

exhaust

fan for the diesel

generator

room

(Section 6.2).

The licensee's

response

to

a violation concerning the use of an automatic

volume control tank makeup valve was not thorough in that appropriate

changes

to an ambiguous

procedure

were not made (Section

9. 1).

~

maintenance

The licensee

performed

an expedient

and detailed review of reactor trip

breaker failure to close problems.

They enlisted extensive

vendor support

and

initiated prompt corrective actions

(Section 4. 1).

Continuing problems. with feedwater

control

system

and steam

bypass

control

valves

caused

operators

to take certain

manual

actions

in response

to .a Unit 2

turbine trip (Section 2.2)

and

a Unit 2 reactor trip (Section 2.3).

The licensee

was slow to initiate a problem evaluation for deficiencies

identified by the inspector concerning control

room essential

air handling

unit bolting (Section 3. 1).

In addition,

a problem evaluation

had not been

initiat'ed in response

to weaknesses

in the maintenance

planning process

which

led to significant rework on the Unit

1 pressurizer

spray valves early .in the

year (Section

10. 1).

In the this case, it appeared

that personnel

involved

assumed

that the current reengineering effort would address

these

weaknesses

without performing

a thorough review.

The licensee

had not established

clear expectations

concerning the practice of

entering the electrical

cabinets for safety-related

equipment.

This

contributed to a situation where both diesel

generators

were inoper able in

Unit 3 when the, plant was shut

down (Section

6. 1).

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En ineerin

The Plant ReviewtBoard

(PRB) performed

a detailed

and proactive evaluation of

a complex issue involving steam generator

tube plug leakage

(Section 3.2).

'The Independent

Safety Evaluation

Group performed

a thorough

assessment

of the

10 CFR 50.59 review program

and identified several

concerns

(Section 8).

Independently,

the

NRR Project

Nanager identified similar program weaknesses

and

a violation concerning the failure to follow the licensee's

10 CFR 50.59

procedure.

Several

good practices

were also noted,

such

as the broad

use of

reference

documents for 10 CFR 50.59 reviews..

The initial review of the auxiliary feedwater

pump trip described

in

Section

5. 1 did not identify the cause of the trip until the inspector

asked

an obvious question in light of the pump's

performance history.

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The licensee

concluded

reviews of reactor coolant

sample valve cracking

and

steam

generator

blowdown water

hammer events.

Both evaluations

were thorough

arid involved considerable

engineering effort. It was noted that the problem

evaluation for the water

hammer event did not initially address

the need to

inform all, operations

personnel

of the efforts needed

to avoid these

events.

~

Hang ement Overview

0

Two areas

of general

concern

were noted.

As discussed

in the plant operations

section

above,

there were two instances

of poor communications

which

contributed to plant events.

The issue of weak communications

practices

as

a

contributor to human performance errors

has

been previously identified.

It

was noted that, in response

to the Unit 2 reactor trip, the licensee

was

establishing

a site wide communication standard.

The report also highlights three instances

in which prnblem evaluations

were

either not initiated for problems or did not cover si g.>ificant attributes

of

the issue.

These

instances

were associated

with:

(1) an evaluation of loose

bolts

on

a control

room essential

ventilation fan (Section 3. 1);

(2) management's

expectations

for entering safety-related

equipment

(Section

6. 1);

and (3)

an evaluation of pressurizer

spray valve maintenance

problems

(Section

10. 1).

Summar

of Ins ection Findin s:

Violations were identified in Sections

5.1

and

8 (Violations 530/9420-01

and 528/9420-05).

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A followup item was

opened in Section

6. 1 concerning

work on diesel

generator

relays

(Inspection

Followup Item 530/9420-02).

A followup item was identified in Section 6.3 concerning the application

of Regulatory Guide

(RG)

1. 108 regarding diesel

generator reliability

testing (Inspection

Followup Item 530/9420-03).

~

A followup item was identified in Section

8 concerning the updates

to'he

final safety analysis report for design

changes

(Inspection

Followup

Item 528/9420-04)

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A response

to

a violation was reviewed

and

was left open (Violation

529/9348-02).

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A violation response

was reviewed

and closed (Violation 528/9348-05).

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A followup item was reviewed

an left open (Inspection

Followup

Item 528/9355-02).

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A followup item was reviewed

and closed

(Inspection

Followup

Item 528/9409-02).

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A followup item was reviewed

and closed

(Inspection

Followup

Item 528/9409-02).

Attachment:

Persons

Contacted

and Exit meeting

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DETAILS

1

PLANT STATUS

1.1

Unit

1

Unit

1 operated

the entire inspection period at essentially

86 percent

power.

The licensee

continued to monitor

a very small primary-to-secondary

leak in

Steam Generator

12 which remained

less

than

1 gallon per day.

S

1.2

Unit 2

Unit 2 began the inspection period at 86 percent

power.

On May 15,

1994, the

turbine tripped

as

a result of a generator field trip (see Section 2.2)

and

'he

reactor

was stabilized at

12 percent

power.

On Nay 16, the unit was

placed

on the grid and achieved

86 percent

power on the next day.

On Nay 28,

the inadvertent

opening of a containment

spray valve caused

a trip of a

reactor coolant

pump

(RCP)

and subsequent

reactor trip (see Section 2.3).

On

June 4, the reactor

was critical and placed

on the grid.

The unit returned to

86 percent

power the next day and remained at that power through the

inspection period.

Unit 3 began. the inspection period in Node

6 with the core reloaded.

The unit

entered

Node

5 on Nay 12.

On Nay 30, after entering

Mode 3 in preparation for

a reactor startup,

a level transmitter nozzle weld on Steam Generator

32 began

leaking.

The licensee

returned the unit to Node

5 to perform

a weld repair.

The licensee

conducted

the repairs

and

on June

7 placed the unit in Node 3.

On June 8, another

Steam Generator

32 weld (on the blowdown sample line) began

leaking

(see Section 2.4).

Again, the unit was placed in Node

5 to conduct

a

weld repair

and ended the inspection period in this mode.

On June

10, the licensee

met with the

NRC for an enforcement

conference

held

at the Region IV office in Arlington, Texas.

The conference

was held to

discuss

the operability of the Unit 3B

EDG and the causes

of the damage

identified in March 1994.

2

ONSITE RESPONSE

TO EVENTS

(93702)

2.1

Fire in the Unit 2 Radiolo ical Controls Area Yard

Re uirin

Notice of

Unusual

Event

On Nay 18,

1994, at approximately 6:40 p.m., the Unit 2 control

room received

notification from security personnel

that

a small fir'e was burning within the

protected

area,

in the radiological controlled area yard.

The Unit 2 fire

team advisor,

a licensed reactor operator,

responded

to the fire.

When the

fire team advisor arrived at the scene,

the fire had

been extinguished

by the

security personnel

with a portable fire extinguisher.

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A preliminary investigation revealed that

a portable light had apparently

fallen or blown over.

The light was

on some plastic covered

plywood.

The

heat from the light ignited

a small section of plastic

and plywood.

The fire

department

removed the plastic

and plywood and hosed

down the area.

Radiation

protection personnel

took air samples

and surveyed

personnel

and materials

as

work progressed

to ensure

there

was

no radiological

problems.

Based

on reports

from the operator

and security department,

the shift

supervisor

determined that the fire had burned longer than

10 minutes,

and

a

Notification of Unusual

Event

(NOUE) was declared

and terminated at 6:48 p.m.,

State

and local authorities

were notified 10 minutes later.

The inspector

observed

the fire area

and concluded that the damage

from the

fire appeared

to be minimal.

The licensee's

emergency'response

has

been

evaluated

in NRC Inspection

Report 50-528/94-19;

50-529/94-19;

50-530/94-19.

2.2.

Unit 2 Turbine Tri

on Loss of Turbine Generator Excitation

On Nay 14,

1994, Unit 2 experienced

a large load rejection when the main

generator

tripped from 86 percent

power.

The genet ator trip occurred

when

an

instrument failure caused

the generator

to lose field excitation.

The loss of

the main generator

resulted in a turbine trip and automatic reduction in

reactor

power to approximately 34 percent

power as designed

by the reactor

power cutback system.

Power

was eventually reduced to approximately

12

percent

by the operators.

The licensee initiated

a condition

report/disposition

request

(CRDR) to evaluate the generator trip and

subsequent

plant and operator

responses.

As operators

attempted to stabilize the plant at 20 percent

power,

steam

generator

water levels developed oscillations of approximately

20 percent of

the narrow range indication.

Operators

placed the feedwater control

system

(FWCS) in manual,

but were unable to control the level oscillations.

The

osci llations increased significantly.

The shift supervisor

decided to reduce

reactor

power from 25 percent to less than

16 percent

(the feedwater

economizer/downcomer

valve swap-over

point).

The

FWCS was returned to

automatic,

power was reduced,

and the level oscillations stopped after swap-

over occurred.

The plant experienced

problems with the steam

bypass control system

(SBCS)

during the plant stabilization.

Valve CV-1001 had

a an erratic response

and

occasionally stuck,

and Valve CV-1004 would not fully close until the valve's

handswitch

was taken to the off position.

The licensee initiated work

requests

to troubleshoot

these valves.

The inspector

noted the continuing problems the licensee

has experienced

with

the

FWCS and

SBCS.

The inspector

noted that problems with the

FWCS and

SBCS

contributed to complications

experienced

following the Unit 2 reactor trip on

May 28,

1994.

The inspector will review the licensee's

CRDR evaluation

as

part of a future routine inspection.

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2.3

Unit 2 Reactor Tri

On Nay 28,

1994, at approximately

11: 15 a.m.,

a reactor trip occurred in

Unit 2 due to a low departure

from nucleate boiling ratio as the result of

RCP

1B tripping following a phase-to-phase

fault.

This fault occurred after

ISC technicians

removed

a relay in the wrong train of the engineered

safety

features

actuation

system,

causing

a containment

spray valve to open

and

borated water to drain from the reactor water tank into the containment

area

where the junction box was located.

The licensee initiated an investigation

of the event to determine the root cause of the errors, to evaluate

the

adequacy of operator

performance,

and to identify and correct

any equipment

problems

caused

by the water in the containment.

On Nay 30,

an

NRC special

team inspection

began

an independent

assessment

of the event.

The results of

the inspection will be documented

in NRC Inspection

Report 50-528/94-23;

50-529/94-23;

50-530/94-23.

Two other minor discrepancies

were identified during the reactor trip event.

First, control

room operators

noted that the rod bottom light and lower

electrical limit light for Control

Element Assembly

(CEA) 3 took approximately

10 seconds

to illuminate after the reactor trip.

Second,

a steam

bypass

control valve and

a feedwater

economizer valve did not go fully shut (slightly

open)

and required operator actions to shut the valve or isolate flow to the

valve.

Regarding the slow illumination of lights on

CEA 3, the operator actions in

identifying the slow illumination of the rod bottom light and initiation of

boration of the. reactor coolant system

(RCS) during the event were

appropriate.

The licensee

reviewed posttrip alarm printouts which showed that

all rods were within 10 inches of each other at the bottom of the core

3 seconds

after the reactor trip, indicating appropriate

response

by CEA 3.

The licensee

investigated

the position indication circuit and tested

the

circuit when the

CEA was actually moved

and could find no cause for the slow

rod bottom and lower electrical limit lights.

A rod drop test of CEA 3 was

conducted

during plant startup to verify proper drop time.

The

CEA met the

test acceptance criteria.

For the steam

bypass control

and feedwater valve problems,

operators

were

aware of prior problems with these

valves

and were able to take manual

actions

to prevent excessive

flow through the valves.

The licensee

performed

a

calibration of the valve positi.oners

and verified proper operation of the

valves prior to unit startup.

While the manual

operator actions to close

valves did not adversely affect operator

response

to this event, there

has

been

a continuing need for operator intervention after plant transients

due to

the failure of these

valves to fully close

when required.

While the licensee

has

been pursuing long-term corrective actions,

minor problems remain.

This

matter warrants

continued

management

attention.

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2.4

Unit 3 Steam Generator

32 Nozzle Leaks

On Nay 30,

1994, while the plant was in No'de 4 in preparation to start

up

following a refueling outage,

the licensee identified

a leaking weld in an

instrument nozzle for the Steam Generator

32 narrow range level instruments.

The nozzle

was welded inside the steam generator,

making inspection

and, repair

difficult.

The licensee

cut out

a segment of the nozzle,

performed

a weld

buildup

on the outside of the steam generator,

and welded

a new nozzle to the

outside of the steam generator.

The licensee

was able to determine through

a combination of ultrasonic,

visual,

and dye penetrant

examinations that neither the nozzle nor the steam

generator

contained

flaws.

The licensee

concluded that the weld must

be the

source of the leak,

although they were not able to directly inspect the weld.

On June 8,

1994, while the plant was in Node 3 following the weld repair, the

licensee identified another leaking weld in Steam Generator

32 in the nozzle

for the downcomer

sample line.

Following the end of the inspection period,

the licensee'inspected

the nozzle weld areas

using

a robot and concluded that

the leaks

were not caused

by the recently performed chemical

cleaning

process

and were probably caused

by inclusions in the weld.

The licensee

indicated

they would remove

and inspect the nozzle weld material in a future outage.

The inspector s will follow the licensee's

actions in the course of routine

inspections.

3

OPERATIONAL SAFETY VERIFICATION

(71707)

The inspectors

performed this inspection to ensure that the licensee

operated

the facility safely

and in conformance with license

and regulatory

requirements

and that the licensee's

management

control

systems effectively

discharged

the licensee's

responsibilities for safe operation.

The methods

used to perform this inspection included direct observation

of'ctivities

and equ'ipment,

observation of control

room operations,

tours of the

facility, inter views

and discussions

with licensee

personnel,

independent

verification of safety system status

and Technical Specifications

(TS)

limiting conditions for operation, verification of corrective actions,

and

review of facility records.

3.'1

Loose Bolts on Control

Room Essential

Ventilation Fan

Unit

1

On Nay ll, 1994, the inspector

noted two loose bolts

on the Train

8 control

room essential

air handling unit fan during a routine plant walkdown.

The

essential

air handling unit was required to be operable

by the plant's

TS to

ensure control

room ventilation and habitability in an accident condition.

The system engineer

inspected

the component

and determined that the fan was

still operable

based

on the fact that ther e were still at least

10 bolts that

were securing the fan to the support saddle.

The inspector

agreed with the

licensee's initial operability determination.

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The licensee initiated

a deficiency work order

(DFWO) to secure

the two loose

bolts.

Additionally, the licensee

inspected all six control

room essential

air handling unit fans

(two per unit) to,ensure all the bolts were tight.

No

other loose bolts were identified.

However, the lic'ensee

noted that there

was

a gap of about 1/8 to 1/4 inch on all the fans

between the flange of the fan

and the fan support saddle.

The installation drawings indicated that the

flange

and the support saddle

should

be flush.

The licensee initiated

a

separate

DFWO to move the support saddle

and ensure that the flange

and

support were flush.,

The inspector

asked the licensee

whether the gap between the flange

and the

support saddle

increased

the shear

stresses

on the bolts.

The licensee

reviewed the seismic analysis of the bolts

and determined that there

was

a

large factor of safety in the analysis

and that any additional

shear stresses

and the two loose bolts would not significantly reduce the margin of safety.

The inspector

concluded that the licensee's

qualitative assessment

of the

structural integrity of the existing bolting configuration was reasonable.

Upon questioning

by the inspector,

the licensee stated that

a

CRDR had not

been initiated because

the evaluation

was adequately

addressed

in the

DFWOs.

The inspector

questioned

the licensee

as to whether

a root cause

analysis

was

conducted to determine

how the bolts

became

loose.

The licensee

conducted

a

search of the work orders

and determined that the fan was last worked in 1987.

At that time, the fan was

removed

and reinstalled.

The licensee

could not

conclusively determine if the bolts were incorrectly installed or if the bolt

nuts

became

loose

due to the gap between the flanges.

Based

on the inspectors

questions,

the licensee initiated

a

CRDR to document the condition of the fans

and the engineering evaluation of the structural integrity of the fan support.

The loose bolts

on the fan were properly aligned

and tightened

on June 9.

The

licensee

had not determined

a schedule to correct the problem with the

gap

between

saddle

and the flange of the fan.

The inspector

concluded that the

licensee

s investigation of the problem was thorough.

However, the inspector

was concerned that

a

CRDR was not promptly initiated. to document all the

actions

and to ensure that the right level of management

was involved in the

issue.

Additionally, the inspector

was concerned that the loose bolts

and the

problem with the gap between the flanges

was not identified earlier.

At the

exit meeting, the licensee

stated that the bolt problem appeared

to have

been

caused

during fan reinstallation in 1987.

3.2

~PRB

II

The inspector

attended

the regularly scheduled

PRB meeting held on Nay 18,

1994 (Neeting 94-17).'he first issue discussed

related to the status of a

welded tube plug in Steam Generator

32.

This tube plug had evidence of

leakage

during the Unit 3. midcycle outage

(December

1993)

and the

PRB

discussed

the issue at

a special

meeting

on December

14,

1993.

During that

meeting,

the

PRB allowed plant restart after reviewing

a safety evaluation

and

qualitative probabilistic risk assessment.

The

PRB reviewed

a plant

memorandum discussing

the Steam Generator

Group's

(SGGs) position that welded

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plugs determined to have through-wall flaws must

be replaced.

Subsequently,

the chairman of the

PRB requested

that the

SGG present their position to the

PRB to determine

whether their position had changed

and

how that affected the

PRB's decision in December

1993 regarding plant restart.

In Heeting 94-17, the

PRB discussed

the

ASIDE Code requirements

(for both

mechanical

and welded plugs)

and

TS requirements

regarding pressure

boundary

leakage

and steam generator

leakage.

The

PRB concluded that,

although not

explicitly addressed

in the code, the intent was that plug replacement

is the

more conservative

course of action

and requested

the

SGG to gather additional

information and report back at

a future meeting.

The

PRB determined that

a

welded plug should

be considered

an extension of the

RCS pressure

boundary

and, therefore,

plug leakage

would be pressure

boundary leakage.

The

inspector

considered this course of action conservative.

Additionally, it was

noted

as

a strength that the

PRB chairman took the initiative'to=. schedule this

discussion

and revisit a previous

PRB decision

when additional information

became available.

This meeting

was evidence of a

PRB that discusses

issues

in-depth

and is proactive in ensuring that the correct decisions

are made.

4

NAINTENANCE OBSERVATIONS

(62703)

During the inspection period, the inspectors

observed

and reviewed the

selected

maintenance activity listed below to verify compliance with

regulatory requirements

and licensee

procedures,

required quality control

department

involvement,

proper use of safety tags,

proper equipment

alignment

and use of jumpers,

personnel

qualifications, appropriate radiation worker

practices,

calibrated test instruments,

and proper postmaintenance

testing.

Specifically, the inspectors

witnessed

portions of the following maintenance

activity:

4. 1

Reactor Tri

Breakers Failin

to Close Durin

Testin

Units 2 and

3

On Nay 25,

1994, the inspector

observed surveillance testing of the reactor

trip paths

per Surveillance Test Procedure

36ST-9SB04,

"PPS Functional Test-

RPS/ESFAS Logic," in Unit 2.

While testing the reactor protection

system

(RPS)

Channel

B trip path, reactor trip switchgear

Breaker

B failed to

close.

The inspector

observed

the technicians'ctions

and concluded that

they appropriately

stopped the test

and notified the assistant shift

supervisor that the breaker

had failed to close.

This event

was followed by

two more occurrences

of reactor trip breakers failing to close.

On Nay 26,

reactor trip switchgear

Breaker

C in Unit 2 failed to close.

Also, on Nay 27,

reactor trip switchgear

Breaker

B in Unit 3 failed to close during testing.

The reactor trip switchgear

breakers,

Westinghouse

Type DS-416,

had recently

replaced

General Electric and other model Westinghouse

breakers

in all three

units.

On Nay 27,

a Westinghouse

representative

arrived at the site

and conducted

an

investigation of the three reactor trip breakers

which failed to close.

It

was determined that the root cause of failure for each of the three breakers

was associated

with the trip latch overlap adjustment

screw.

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the vendor concluded that the normal four turns of the overlap adjustment

screw did not provide enough overlap of the trip latch onto the trip shaft for

these

breakers.

As

a result, vibration

induced

when the closing springs

were

energized to close the breaker

caused

the trip latch to trip free, thereby

leaving the breaker in a tripped condition.

The vendor

recommended

that the normal four full turns of the breaker trip

latch overlap adjustment

screw

be increased

to a limit of five full turns

when

required.

This additional overlap reduces

the mechanism's

sensitivity to

vibration and prevents

the breaker

from tripping free during the closing

stroke.

On June

1, the licensee

received

a letter from Westinghouse

authorizing the additional full turn.

Westinghouse

also provided additional

testing requirements

to insure that increas'ing the .overlap does not prevent

the breaker

from opening

on demand.

The inspector

reviewed these testing

requirements

and concluded that they provide assur ance that the increased

overlap will not affect the ability of the breaker to open

on demand.

The

licensee

planned to incorporate these requirements'into

Procedure

32NT-9SB03,

"Naintenance of Westinghouse

Type DS-416 Reactor Trip Switchgear."

Test results

on the three reactor trip breakers

showed that the five-turn

adjustment corrected

the observed trip free closing condition.

In addition,

the response

times remained within acceptance criteria and the shunt

trip/undervoltage trip gaps were not increased.

The licensee

replaced

the two

Unit 2 breakers,

but the replacement

breakers

did not require more than four

full turns of the overlap adjustment

screw.

The Unit 3 breaker

was adjusted

to 5 turns

and returned to service.

The licensee

planned to adjust the other

- reactor trip switchgear

breakers

as required,

during future routine preventive

maintenance.

The inspector

concluded that the licensee

performed

an expedient

and detailed review of reactor trip breaker failure to close problems,

involving extensive

vendor support,

and initiated prompt corrective actions.

5

SURVEILLANCE OBSERVATION

(61726)

The inspectors

reviewed this area to ascertain that the licensee

conducts

surveillance of safety-significant

systems

and components

in accordance

with

TS and approved

procedures.

5. 1

Auxiliar

Feedwater

Pum

Overs

eed Tri

Durin

Testin

- Unit 3

,

On June

8, at approximately 5:30 a.m., turbine-driven auxiliary feedwater

Pump AFA-P01 tripped

on mechanical

overspeed

during surveillance testing

when

the Unit was in Node 3.

After the

pump trip, the licensee

declared

Pump AFA-

P01 inoperable

and entered

a 72-hour

TS action statement.

The licensee

established

the, normal

steam pressure

to test the

pump at approximately

4 a.m.

on June 8.

The inspector

reviewed the surveillance test procedure

and the normal

operating

procedure for Pump AFA-P01, attended

a meeting with operations

and

engineering to determine the cause of the overspeed trip, and discussed

the

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event with plant supervision.

The licensee

concluded that the trip was caused

by steam

condensing

when it contacted

a relatively cold supply line and

entered'the

pump turbine.

The inspector

noted the following weaknesses

concerning the event:

Poor communications

between operators

led to inappropriately starting

Pump AFA-P01 with a cold steam supply line.

~

The licensee's

investigation of the event did not promptly determine the

temperature

of the steam lines prior to starting

Pump AFA-P01.

As a

result, the licensee

was slow to determine the root cause of the event.

The steam supply for Pump AFA-P01 is provided from two main steam lines

through separate

steam supply lines.

Each supply line has

an isolation valve

(SG-134

and SG-138) located near the main steam line.

These isolation valves

have small

bypass lines with solenoid operated

valves.

These valves are

normally closed

when the

pump is in standby.

The two lines travel to the room

for Pump AFA-POl, where they are joined.

The licensee

had previously identified that condensation

has occurred during

a

pump start

when the isolation valve was opened

and steam

was exposed to the

cold portion of the steam supply line.

The licensee

had found that the

turbine governor could not compensate

for the resultant water "slug" which has

caused

Pump AFA-POl to overspeed.

To address this, the licensee

has taken the

position that

Pump AFA-P01'as only operable with the temperature

of the

downstream portion of the steam supply lines greater

than 190'F.

In the past,

there

has

been sufficient leakage

past the isolation and bypass line valves to

keep the lines warm.

The licensee

also installed

an on-line temper ature

monitoring system

so that temperature

could be verified during operator

rounds.

The licensee

investigated

the June

8 overspeed

event

and determined that

communications

weaknesses

were

a significant contributing factor.

Prior to

starting the surveillance test of Pump AFA-POl, the primary reactor operator

noted that the procedure

did not have any limitations for the temperature

of

the steam supply piping prior to starting the pump.

The reactor operator

(RO)

asked the assistant shift supervisor if the minim'um supply line temperature

of

193'F (described

in the normal operating procedure)

applied during the

performance of the test.

The assistant shift supervisor

noted that the

precaution section of the operating

procedure

stated that the steam supply

line temperature

was required to be greater

than

193~F.

The assistant shift

supervisor

then apparently

answered

"yes" to the RO's question concerning

whether the temperature limit applied to the test. The

RO thought that the

assistant shift supervisor

had actually verified that the supply line

temperature

was greater than 193'F.

The assistant shift supervisor

had not

verified the temperature,

and the actual

steam line temperature,

as measured

by the temperature

monitoring recorder,

was 77'F.

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After this discussion,

the

RO opened the Train A steam supply Valve SG-134

and

started

AFA-POl.

The

pump turbine reached

rated

speed of 3600 rpm and the

governor

was properly controlling turbine speed.

The operators

ran the

pump

for about

40 minutes

and then opened the Train

B steam supply Valve SG-138

as.

directed

by the test procedure.

As soon

as Valve SG-138 opened,

the turbine

slowed to 3400 rpm and then its speed

increased

quickly, which caused

a

mechanical

overspeed trip.

The inspector

noted that the test procedure for Pump AFA-POl required that the

operators verify system line-up in accordance

with the normal operating

procedure.

The normal operating

procedure

had precautions

to ensure that the

temperature

of the steam supply line was greater

than 193'F using either the

on-line temperature

recording

system or a hand held pyrometer prior to

starting the

pump.

The inspector

concluded that not ensuring the temperature

of the steam supply line was greater

than 193'F prior to starting the

pump was

a failure to follow procedures

(Violation 530/9420-01).

During the event investigation,

the licensee

did not establish that the steam

supply'ad not been adequately

warmed until the inspector

asked

what the

temperature

had

been prior to the

pump start.

The inspector

posed the

question following two licensee staff meetings,

which included plant

management

and engineering

involvement

and substantial

exploration of the

cause of the overspeed

condition.

Based

on the inspector's

question,

the operations

supervisor

then reviewed the

auxiliary operator

logs

and noted that the temperature

'was logged

as 77'F.

The auxiliary operator

had circled the reading

as "out of specification"

and

made

a comment

on the log sheet that the reading

was low due to not being at

normal operating

steam pressure.

The inspector

expressed

concern regarding the need to prompt the licensee

regarding the initial steam line temperature

given the history of overspeed

trip events

due to condensation

and the relatively short time between reaching

normal operating temperature

and starting the

pump.

The inspector

noted that

the appropriate individuals had

been involved in the event, review.

However,

it appeared

that these individuals had relied on assumptions

rather than the

evidence available in performing their initial review.

The inspector

concluded that, while those involved may have ultimately determined

the

correct root caus'e,.their initial review was not well conducted.

The licensee initiated

a

CRDR to document the event

and to evaluate

the

operator

communication errors which led to the event.

Plant engineering

had

initiated

a review of the adequacy of the design of the steam admission

system

to prevent water intrusion into the tur bine following concerns

raised

by the

testing

NRC team inspection

(NRC Inspection Report 50-528/94-12;

50-529/94-12;

50-530/94-12).

The details of the recent

overspeed trip event were included

in this evaluation which was scheduled to be completed

by the end of June.

A

review of this evaluation will be conducted

in a future inspection.

J

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'.2- Other Surveillances

Observed

The inspectors

observed portions of the following surveillances

and determined

that they were performed acceptably:

42ST-2SGOl

Nain Steam Line Isolation Valves Surveillance 4.7. 1.5

42ST-2DF01 Diesel

Fuel Oil

Pump Operability 4.0.5

6

DIESEL GENERATOR PROBLENS

(62703,

61726)

6. 1

Rela

s Not Full

Inserted

Unit 3

On Nay 17,

1993, the Unit 3 control

room received

a trip alarm and

a high

priority alarm on

EDG 3A while the unit was in Node 5.

Because

the Train

B

diesel

generator

was inoperable

due to maintenance activities, the licensee

entered

the

TS action statement for having no diesel

generators

available.

Followup investigations

by the licensee

concluded that

EDG 3A would have

been

available in the emergency

mode.

The inspector

reviewed the licensee's

immediate actions

and concluded that they were appropriate.

The licensee

found that two power relay and controls technicians

had entered

the

EDG 3A control cabinet to trace wiring in preparation for work they

intended to perform later that day.

The technicians

did not have control

room

permission to perform the work, but intended to obtain the permission

following their wire tracing.

Mhile in the cabinet,

one of the technicians

caused

a poorly seated relay to break contact with its socket,

which caused

the alarm.

The licensee initiated an investigation

and discovered that

some of the

Agastat relays,

including the one that caused

the alarm, were not fully

inserted into their respective

sockets.

The circuit that caused

the alarm

reportedly fell out of the socket

when the personnel

removed the seismic

restraint.

The licensee

discovered that

some of the relays that were

purchased

were commercial

grade

and

had

an injection mold lip at the bottom of

the relay which made the relay difficult to insert into the socket.

The licensee

also reviewed the circumstances

surrounding the technicians

entering

a cabinet for the remaining available

EDG without permission

from the

control

room operators.

The licensee

discussed

the preliminary findings and

corrective actions with the inspector

and indicated that this was probably

an

isolated occurrence.

The licensee

noted that the two individuals involved

have

been counselled

and that the power relay and control,s organization

has

had 'subsequent

training concerning e'ntering safety-related

equipment without

permission.

The inspector questioned

the licensee

as to whether they had established

an

expectation for when plant personnel

can

and cannot enter cabinets for safety-

related

equipment without permission.

The inspector discussed

with members of

the unit staff their practices for entering safety-related

equipment cabinets

and discovered that there

was

no consistent

known management

expectation.

l

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Some individuals believed that it was acceptable

to open

and enter

a safety-

related cabinet without permission

as long as

no work was being performed,

while others

believed tPat they should obtain permission to open

any

cabinet/drawer

(safety-related

or nonsafety-related).

The inspector

discussed

the need to develop

a consistent

policy for opening

safety-related

equipment cabinets

and to disseminate this policy to the

employees.

At the exit meeting,

the licensee

stated that they would review

their position

and ensure that the appropriate

individuals were provided

guidance.

The inspector will review the licensee's

corrective actions to

develop

and disseminate

a policy regarding entering safety-related

equipment

and the results of the rel'ay insertion problem when the investigation is

complete (Inspection

Followup Item 530/9420-02).

6.2

Diesel

Generator

Exhaust

Fan Ino erable

Unit 2

On Nay 13,

1994, Unit 2 was in Node I when members of the

PRB determined that

the

EDG 2B had

been inoperable

from approximately 4:48 a.m.,

on Nay 10, to

approximately 8:55 a.m.,

on Nay 13.

For approximately

76 hours8.796296e-4 days <br />0.0211 hours <br />1.256614e-4 weeks <br />2.8918e-5 months <br />, the Train

B

EDG building essential

exhaust

fan had

been

removed

from service with its

breaker in the open position

and with the fan's discharge

damper wired in the

closed position.

The

PRB determined that the exhaust

fan had not been capable

of performing its specified support function.

The essential

exhaust

fan

starts automatically when the

EDG starts to ensure sufficient room cooling and

is considered

necessary

attendant

equipment required for the

EDG to perform

its intended safety function.

On Nay 10, operations

personnel

evaluated

opening the essential

exhaust

fan

breaker to support. preventive maintenance

on the exhaust

fan screen.

They

determined that the operability of the

EDG was not impacted

because

the

essential

exhaust

fan could

be reenergized

and manually started

should

EDG

operation

be required.

Operations

personnel

failed to consider the essential

exhaust

fan as necessary

attendant

equipment that was required for the

EDG to

perform its intended safety function.

Subsequently,

maintenance

workers wired

the fan's discharge

damper shut to serve

as

a foreign material

boundary.

This

step

was not communicated to the operators.

The inspector

noted that this event

was similar to another

example of where

the licensee

removed

a system

from service that had

an automatic design

function to support the

EDG without an operability evaluation

(see

NRC

Inspection Report 50-528/94-02;

50-529/94-02;

50-530/94-02).

Previously the

licensee isolated the jacket water expansion tank automatic make-up valve in

Unit I, an automatic function described

in the Updated Final Safety Analysis

Report

(UFSAR).

The licensee

submitted

Licensee

Event Report 94-001-00

as

a result of the

EDG

and attendant

equipment

being inoperable

for. greater

than

72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />.

The

inspector will evaluate this event

and the licensee's

actions in a future

review of the licensee

event report.

1

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-16-

0

6.3

Application of RG 1.108 Regarding Valid Tests

and Failures

On June

2,

1994, the licensee

discussed their interpretation of RG 1. 108,

regarding diesel

generator reliability testing, with the inspector,

the Office

of Nuclear Reactor Regulation

(NRR) Project Nanager,

and the Chief of the

Electrical Engineeting

Branch,

NRR.

The licensee

had concluded that only the

monthly diesel

generator

surveillance tests

should

be included

as valid tests

under

RG 1. 108.

The inspector

and

NRR concluded that all surveillance tests,

not just the monthly surveillance tests,

should

be included

as valid tests.

The licensee

committed to reassess

their position

and evaluate

the impact on

the reliability trends of the diesel

generators.

On June

6, the licensee

informed the inspector that they had not included

several

diesel

generator tests

as valid tests

because

the start times of the

diesels

had not been recorded.

The licensee

observed

and the inspector

concurred,

that

RG 1. 108 did not include start times

as

a criteria for

recording valid tests.

The licensee

committed to reassess

this issue

and to

evaluate the impact on the reliability trends of the diesel

generators.

The

inspector will review the licensee's

evaluation in a future inspection

(Inspection

Followup Item 530/9420-03).

7

CONTAINMENT PENETRATION TESTING AND VALVE LINEUP Unit 3

(61715)

The inspector

conducted

a review of the licensee's

testing

and procedures

to

verify that the

TS requirement to maintain primary containment integrity prior

to entering

Node 4 operations

was satisfied in Unit 3.

The inspector

conducted

the review while Unit 3 was in Node

5 at less than 210'F.

The inspector

reviewed the local leak rate test

(LLRT) results of selected

mechanical

and electrical penetrations,

verified the operability of the

CS

system,

reviewed the basis for the surveillance test

(ST) procedure for

ensuring that manual

valves associated

with containment penetrations

are

verified closed,

and observed the

LLRT of the containment

personnel

airlock.

The inspector

concluded that all the penetrations

that were required to be

tested successfully

passed

an as-left

LLRT.

The inspector also noted that the

testing of the personnel

airlock was appropriately conducted.

The inspector

noted that all the required tests to verify operability of the

CS system were

satisfactorily completed

and appropriately reviewed.

The inspector identified several

manual

vent and drain valves in penetrations

that were Type

C leak tested that were not verified closed

as part of the

containment integrity ST.

The licensee initiated

a review of the

ST procedure

and determined that the

ST met the intent of the TS.

However, the licensee

also noted several

inconsistencies

in the procedure

and was conducting

a

detailed evaluation of the design basis for verifying containment integrity.

The inspector

agreed with the licensee's

conclusions

and noted that the

licensee initial response

to the inspector's

questions

was

good.

A discussion

of the details of this finding follows.

~ ~

-17-

7.1

Verification of Containment

Vent and Drain Valve Positions

The inspector

reviewed

Procedure

43ST-3ZZ13 "Containment Integrity-

penetrations

4.6. l.la."

The purpose of the procedure

was to meet

TS 4.6. l.l.a

which requires that primary containment integrity shall

be demonstrated,

"at

least

once per 31 days

by verifying that all penetrations

not capable of being

closed

by OPERABLE containment

automatic isolation valves

and required to be

closed during accident conditions are closed

by valves, blind flanges,

or

deactivated

automatic valves secured

in their actuated

position except

as

provided in Table 3.6. 1."

The inspector

reviewed the

UFSAR to determine which penetrations

have valves

that would receive

a containment isolation actuation signal,

a containment

spray actuation signal,

or

a containment

purge isolation actuation signal to

shut during an accident condition.

The inspector

determined that all the

manual

vent and drain valves connected to penetrations

that received

a

containment isolation actuation signal,

a containment

spray actuation signal,

or a containment

purge isolation actuation signal

were included in the

ST

procedure.

The inspector

noted that the

ST procedure

also included manual

vent

and drain

valves associated

with penetrations

that were listed in the

UFSAR and .the

TS

as containment isolation valves that were required to be open during accident

conditions.

Even though these penetration

were required to open, they were

Type

C tested to ensure that the isolation valves were leak tight.

Based

on

this observation,

the inspector

reasoned

that penetrations

that were Type

C

tested to ensure .the leak tightness of the penetration

should also have the

manual

valves verified shut in the ST.

To verify this assumption,

the

inspector

reviewed the valve configurations for all the penetrations

that were

Type

C tested

and identified four manual

vent and drain valves associated

with

the shutdown cooling

(SDC)

and the .high pressure

safety injection (HPSI)

system long-term recirculation path penetrations

(penetrations

26, 27, 67,

and

77)'hat were not verified closed in the ST.

7.2

Licensee

Evaluation

The inspector

discussed

the apparent

omission of the manual

vent and drain

valves associated

with the

SDC and

HPSI long term recirculation valves with

the shift operations

crew.

The licensee initiated

CRDR 3-4-0331 to evaluate

the condition and determined that the manual

valves connected to the

penetrations

in question

(26, 27, 67,

and 77) were not required to comply with

TS 4.6. l.Ia.

The basis for the licensee's

determination

was that the valves

were connected to penetrations

that were required to be open during, accident

conditions

and

TS 4.6. 1. la applied to valves that were required to be closed

during accident conditions.

Additionally, Section 6.4.2. 1 of the Combustion

Engineering standard

safety analysis report stated that the

SDC and safety

injection systems

were considered to be an extension of the 'containment

pressure

boundary.

Therefore,

containment integrity would be verified by

ensuring the. integrity of the safety injection and

HPSI systems.

The

3

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-18-

inspector

agreed with the licensee's

conclusion that the

SDC and

HPSI long-

term recirculation penetrations

were not required to be checked to meet the

intent of the TS.

The licensee

reviewed the configuration

and design

basis for all the

mechanical

penetrations

and did not identify any manual

valves that should

be

verified to meet the intent of the

TS that were not included in the ST.

However, the licensee

did identify several

other penetrations

that were

required to be open during accident conditions that had the vent and drain

valves verified shut in the

ST procedure.

The licensee

was reviewing the

design basis for all the penetrations

that were required to be open to

determine if the vent

and drains should

be included in the

ST or in other

operations

procedures.

The inspector will review the results of the

CRDR

during an ongoing inspection of containment integrity.

8

DESIGN CHANGES IN ACCORDANCE WITH 10 CFR 50.59

(37001)

The inspector

reviewed the licensee's

procedures

and training records for

conducting

10 CFR 50.59 evaluations.

The inspector

found that the procedures

were generally well written and contained

adequate detail.

The inspector also

found that the qualification requirements

for personnel

who screened,

evaluated,

and reviewed

10 CFR 50.59 evaluations

were significant in terms of

experience

required

and factored in increasing

requirements

for the evaluator

and reviewer positions.

The inspector

learned that no requalification

training was required for personnel

performing

10 CFR 50.59 screenings

and

evaluations

and pointed out that Procedure

01PR-ONS04 clearly presumed

a

requalification program.

The licensee

stated that

an internal

assessment

had

identified

a similar finding regarding requalification training,

and the

finding was being evaluated.

The inspector reviewed the previous

two assessments

of the

10 CFR 50.59

program performed

by the licensee

and

had no comments

on the first assessment,

performed in November

1991.

The second

assessment

had recently

been

completed

(April 1994)

by the site's

Independent

Safety Evaluation

Group (ISEG).

Although the assessment

report was not yet complete,

the inspector

reviewed

the team's

summary slides

and found that the assessment

appeared to be

thorough

and documented

several significant findings.

One finding was that,

from the screenings

sampled,

approximately

30 percent of the negative

screenings

(meaning

a

10 CFR 50.59 evaluation

was not necessary)

should

have

been positive.

The inspector

reviewed several

of the deficient screenings

and, in general,

concurred with the

ISEG assessment.

As

a result of ISEG's

.finding,

a

CRDR was generated

to perform the

10 CFR 50.59 evaluations for the

deficient screenings

and to perform

a root cause evaluation of this weakness.

The inspector

reviewed the licensee's

10 CFR 50.59 annual report of plant and

procedure

changes,

dated

June

24,

1993,

and selected

approximately

20 change

packages

from a variety of procedure,

design change,

and modification

categories

for a detailed

review.

In general,

the inspector

found that the

summaries

provided in the

10 CFR 50.59 annual report were adequately detailed

l

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in describing the change to the facility or procedure.

The inspector verified

'that only qualified individuals performed the

10 CFR 50.59 screenings

and

evaluations.

Overall, the inspector

found that the

10 CFR 50.59 evaluations

adequately

supported

the conclusions that were drawn.

An overall strength

was the

extensive listing of licensing basis

documents that were reviewed in preparing

the evaluation,

which indicated

a strong

commitment to ensure that facility

changes

were properly evaluated.

Several

design

changes

were reviewed that had two 10 CFR 50.59 evaluations

(one for plant operations

and

a separate

evaluation for plant implementation).

Although these evaluations

could be combined, this approach

was considered

a

strength

because

the operations

evaluation could focus

on the various system

and equipment requirements

for different operational

modes,

and the

implementation evaluation could focus

on other concerr

<. (e.g.,

shutdown risk

factors).

The inspector

reviewed approximately

seven

design

change

packages

to verify

that drawings

and

UFSAR sections

were updated.

The inspector

found that the

UFSAR had not been

updated for two design

changes

which had

been

completed in

Narch

and August 1993.

The licensee initiated a

CRDR to review each closed

design

change

package for the last several

years to identify any changes that

have not been incorporated into licensing basis

documents.

The inspector will

review the licensee's

CRDR in a future inspection report (Inspection

Followup

Item 528/9420-04).

One of the de'sign

change

packages

reviewed,

PJ-Sg-065,

provided for

functional separation

of the condenser

exhaust effluent radiation monitors,

by

rerouting the condenser

exhaust to the plant vent.

The

10 CFR 50.59 screening

correctly identified that the

TS were affected (Figure 5. 1-3 depicts

a

separate

release

path for the condenser air removal

system);

however, the

evaluation

was performed

and the modifications were completed

on all three

units prior to a TS change

being submitted

and approved

by the

NRC.

Although

the significance of the required

TS change

was low in that it involved a

change to a TS figure, procedure

93AC-ONS01

"10 CFR 50.59 Screening

and

Evaluation,"

was not followed.

The failure to follow procedures

is

a

violation (Violation 528/9420-05).

Evaluations that lacked information or wei e not adequately detailed

included

the following:

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Temporary Nodification 89-CP-076

removed

handwheels

for four containment

purge valves,

but the evaluation did not address

whether

manual

operation of the valves

was

assumed

in the

UFSAR or emergency

procedures.

Design

Change

package

NC-041 upgraded

valve operator motors

and gear

sets

on two nuclear cooling water containment isolation valves.

The

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design

package only stated that the

TS requirements

were not affected

and did not discuss

the potential

impact of too fast of a stroke time on

valve reliability or system response.

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Limited Design

Change

Package

RJ-048

implemented

a core operating limit

supervisory

system software

change to automate the monitoring of the

Azimuthal

Power Tilt TS limit.

The

10 CFR 50.59 screening

indicated

that the change did not involve a test

described

in the

UFSAR; however,

the screening

referenced

a preoperational

test of core operating limit

supervisory

system, defined'in

UFSAR Section

14.2. 12, to verify proper

system operation.

moreover,

the evaluation

used conflicting logic in

answering questions

regarding

an increase

in either the probability or

consequences

of an accident.

In each case,

the inspector discussed

the evaluation with cognizant licensee

personnel,

reviewed applicable

documentation

and test results,

and determined

'hat the changes

were either

bounded

by existing analysis

or did not affect

safety.

9

FOLLONlP OPERATIONS

(92901)

9.1

0 en

Violation 529 9348-02:

Failure to Follow Procedures

for RCS

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This violation involved the failure to return the reactor

makeup water

controller to automatic following a dilution evolution.

On November 23,

1993,

the inspector noted shortly after shift turnover that the reactor

makeup water

controller was in manual.

The procedure directed the operator to place the

controller in automatic following manual operation.

The primary operator

subsequently

placed the controller to automatic

when informed by the

inspector.

The inspector reviewed the licensee's

response

to the violation and noted that

the licensee's

corrective actions

included

an operations

management brief

given to each

crew on the incident and management's

expectations

for

procedural

adherence.

In addition, positive discipline was administered to

the individual involved in the event.

R

On Nay 9,

1994, the inspector

observed that the Unit 2 reactor

makeup water to

volume control tank flow controller

(CHN-FIC 210X) was in manual.

Mhen asked,

the

RO stated that

he chose to leave the controller in manual

because

he was

performing

an

RCS dilution every 45 to 60 minutes.

The inspector

asked the

RO

if he was

aware of a previous Unit 2 violation for not lining up the makeup

system for automatic operation.

The

RO responded that he was unaware of any

previous event involving the reactor

makeup system.

The

RO reviewed the

chemical

and volume control system

(CVCS) normal operations

procedure

(420P-

2CH01)

and subsequently

returned the flow controller to automatic.

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The inspector

discussed this with Unit 2 operations

management.

Operations

management

stated that it was their expectation that, if an evolution,

such

as

dilution of the

RCS,

was performed

on

a relatively frequent basis, it

was'cceptable

for the operators to leave the flow controller in manual after the

completion of the dilution and not return the controller to automatic.

In

addition, operations

management

stated that they expected

the operators

to

return the controller to automatic prior to shift turnover or document in the

shift turnover log that the controller was left in manual.

The inspector

noted that this interpretation

was consistent with the licensee's

discussion

in their response

to the previous notice of violation.

In response

to the

RO not being aware of the previous violation concerning

reactor

makeup system,

the licensee

generated

a

CRDR to determine

how

information and actions that are taken to resolve previously identified

concerns

are communicated to department

members

and to determine if these

methods

are adequate

to prevent similar occurrences

in the future.

The

licensee

subsequently

determined that the operator

had received training on

management's

expectation

regarding the flow controller, but did not remember

the training.

The inspector

noted that, inthe response

to the violation, the licensee

did

not identify any procedural

problems.

The inspector

reviewed Procedure

420P-

2CHOl and concluded that management's

expectation

concerning the flow-

controller

was unclear.

Following the Nay 9 event,

the licensee

generated

a

temporarily approved

procedure

action

(TAPA) to direct operators

to line up

the makeup system for automatic or manual operation per the shift supervisor's

or assistant shift supervisor 's direction.

The inspector

concluded that this

revision allowed operators

the option to leave the controller in manual;

however, it did not clarify management's

expectation for returning the

controller to automatic prior to shift change or document the condition during

turnover.

The inspector

reviewed the

CVCS normal operations

procedures

for all three

units

and discovered that only the Unit 2 procedure

had

been revised to

incorporate the TAPA.

The licensee

indicated that the Unit

1 and Unit 3

procedures

would not be changed until the next procedure revision in early

1995.

The inspector questioned

the specific individual responsible for the

CVCS normal operations

procedure

and discovered that

he was not aware that the

procedure

change resulted

from a violation.

The licensee

changed their

priorities and decided to issue the procedure revisions incorporating the

TAPAs.

This violation will remain open until the inspector reviews the

procedures

to ensure the change is incorporated.

9.2

Closed

Violation 528 9348-05:

Inadvertent

RCS Draindown

This violation involved the inadvertent draining of the

RCS level from the

reactor vessel

flange level (about

114 feet) into the reduced

inventory level

(< 111 feet)

on November 3,

1993, while the plant was in a refueling outage.

The primary reactor operator

performing the evolution was distracted

during

the evolution and did not monitor the

RCS level for approximately

8 minutes.

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The licensee initiated several

immediate corrective actions,

documented

in NRC

Inspection

Report 50-528/93-48;

50-529/93-48;

50-530/93-48,

and discussed the,

broader

performance

issues

surrounding the event at

an

NRC management

meeting.

One of the key issues

the licensee

emphasized

at the meeting

was that shift

supervision

allowed important evolutions to be conducted without maintaining

expected

communication standards.

To address this issue,

the licensee

scheduled'igh

intensity training (HIT) in the simulator.

This training was

designed to improve team communication skills.

The inspector

observed

portions of the HIT and found that it emphasized

both communications

and

teamwork

(see

NRC Inspection Report 94-09).-

The inspector also noted that, during the Unit 3 steam generator

inspection

outage in December of 1993

and the Unit 2 midcycle outage in January

1994,

an

alarm was installed that would annunciate

when the

RCS level

was less than

ill feet.

The inspector noted that this alarm and the previous corrective

actions

should prevent

a similar problem with inadvertently draining the

RCS.

The inspector

noted that management's

efforts to improve crew communications

needed to continue

based

on recent errors in Units 2 and 3.

For example,

poor

.communications

between operators

and technicians

in Unit 2 contributed to

inadvertently opening

a containment

spray valve and

a reactor trip (see

paragraph 2.3).

In Unit 3, weak communications

between operators

resulted in

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starting the turbine-driven auxiliary feedwater

pump with cold steam lines.

This resulted in an overspeed trip of the turbine due to.condensation

in the

steam lines

(see

paragr aph 5. 1).

The inspector will continue to monitor communications to ensure that

communications

during control

room evolutions

are precise

and meet

management's

expectations.

10

FOLLOWUP NAINTENANCE

(92902)

10. 1

0 en

Ins ection Followu

Item 528 9355-02:

Pressurizer

S ra

Valve

Naintenance

This open item involved the engineering resolution of repeated

problems with

maintenance

on the pressurizer

spray valve air operators

in Unit l.

Specifically, the inspector

was concerned

about apparent

weaknesses

that

prevented

engineering

information from being factored into the maintenance

work orders.

The- licensee identified two factors that contributed to the work order not

referencing current engineering

information regarding the pressurizer

spray

valve air operator

bench set.

The first problem was that the revised

bench

'set pressures

were not incorporated into the engineering

comments

screen

in

the component information computer data

base.

The second

problem was that the

revised

bench set pressures

that had

been incorporated into a preventative

maintenance

(PN) task

had not been carried over into a maintenance

task that

replaced

the

PN task.

The licensee

concluded that the distribution of

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information between

engineering

and the work planners

should improve with the

maintenance

team concept

being implemented

as part of the reengineering

effort.

The inspector

noted that the licensee's

evaluation of the communication

problems

was not incorporated into the formal

CRDR evaluation

process.

Additionally, the licensee

did not address

the reasons

why the information

screen

was not updated

and if there were other

PN tasks that were converted to

maintenance

task with inadequate

or missing information.

The licensee

believed the reengineering

process

would prevent these errors in the future

without understanding

the specific barriers to ensure that information was

properly incorporated into work documents.

The licensee initiated

a

CRDR to

address

these

issues.

This item will remain

open pending the inspector's

review, of the licensee's

CRDR.

ll

FOLLONJP ENGINEERING/TECHNICAL SUPPORT

(92903)

11. 1

RCS

Sam le Valve Crackin

In NRC Inspection

Report 50-528/94-02;

50-529/94-02;

50-530/94-02,

the

inspector discussed

the licensee's

discovery of cracks in two Unit 2

RCS hot

leg sample line valves

(SSAUV-203 and SSBUV-200).

At the end of the

inspection period, the licensee

had not determined the cause of the cracks.

The licensee

subsequently

determined the cause of the cracks

and has initiated

appropriate corrective actions.

The

RCS sample valves were supplied

by Valcor Engineeri.ng Corporation

and were

essentially stainless

steel

blocks weighing approximately

40 pounds.

Inlet

and outlet ports were drilled into the valve body.

Additionally, a larger

diameter cylindrical area

was provided for a threaded

bonnet

and the valve

internals.

The cracks circumscribed the seat

area at the base of the larger.

cylindrical area.

Additionally, cracks were found initiating from areas

of

stress

concentrations

at the inlet and outlet ports.

The licensee

determined that the cracks

were caused

by thermal cycling.

The

normally closed valves were routinely opened to draw samples

from the

RCS.

This resulted in thermal cycles from approximately

100'F to 600'F.

This

caused

high stress,

low cycle fatigue.

The licensee

determined that

sufficient thermal stress

was created

during valve heat

up to compressively

yield the material.

The licensee

evaluated

the cracks to determine if.it had affected the

operability of these

valves

and other similar valves.

The licensee

concluded

that operability was'ot affected.

The licensee

determined that, at the

present rate of growth, the cracks would not affect valve integrity for at

least

5 years of operation.

Additionally, the Unit 2

RCS hot leg sample

valves

had experienced

the greatest

number of thermal cycles.

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Inspections of Unit 3 valves were performed during the refueling outage.

The

licensee

discovered that both

RCS hot leg sample valves exhibited similar

cracking.

Additionally, they discover ed that

a sample valve for the

pressurizer

steam

space

(SSA

UV 205)

had crack indications.

The licensee

estimated that this particular valve would have experienced

I/10th of the

number of cycles

as the hot leg sample valves

and speculated

that the crack

depth would be proportionally shallower.

At the end of the inspection period,

the licensee

was examining the valve to determine the depth of these

indications.

In response

to the inspector's

questions,

the licensee

reviewed their

purchasing

documentation

and determined that the purchase

order for the

RCS

sample valves specified

maximum temperature,

but did not indicate that the

valves would be exposed to thermal cycles.

The inspector

asked if the vendor

would have provided these particular valves if the purchase

order

had

indicated- exposure to thermal cycles.

The licensee

indicated that the vendor

stated that the valve is an excellent design

and is appropriate

even in a

thermal cycling application.

Also, the vendor stated that cracks

have not

been

observed

in similar valves at other nuclear facilities.

The licensee

investigated

the nuclear plant reliability data system data

base

and found no similar failures.

They also discussed this with other licensees

identified in the nuclear plant reliability data

system data

base

and found

that none

had

used these valves in similar applications.

The licensee

also

discussed

these findings on the Nuclear Network.

The inspector

found these

actions to be appropriate.

11.2

Closed

Ins 'ection Followu

Item 528 9409-02:

Steam Generator

Blowdown

S stem Water

Hammer Event

This item concerned

a water

hammer event in the Unit I steam generator

blowdown system which occurred

when the blowdown system containment isolation

valves were opened to return the blowdown system to operation.

The blowdown

system

had

been depressurized

for maintenance.

The inspector

noted that the operating

procedure for the system included

a

caution that

a water

hammer could occur when opening the containment isolation

valves.

The inspector

was concerned that this step indicated that water

hammers in the blowdown system

may be routine and that appropriate corrective

actions to prevent the water

hammer events

had not been taken.

In addition,

the inspector questioned

whether the licensee

had evaluated

the hydraulic

impact on the system

components.

The licensee

reviewed the available work history to determine the last time

a

blowdown system water

hammer

had occurred.

They determined that the most

recent event

had occurred in mid-1990 and that the procedure caution

had

been

added to following the event.

The system engineers

recalled similar events

during initial plant startup.

They also identified

a modification, which had

been in a hold status,

to modify the blowdown system to prevent

a water

hammer

event.

The inspector

concluded that these

events

appeared

to be infrequent.

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The licensee

performed

an evaluation of the stresses

placed

on the blowdown

system during the water

hammer event.

They determined,

based

on the force

required to cause

the

damage to the pipe supports,

that the forces

had not

exceeded

the allowable forces for the system.

The licensee initiated

a design

change request to modify the system to include

a bypass line, with three series isolation valves,

around the outboard

containment isolation valves in all three units.

The licensee

plans to revise

the procedure for returning the blowdown system to operation to require that

the bypass line be opened to equalize

system pressure prior to opening the

containment isolation valves.

The licensee

planned to expedite this

modification in all units.

The inspector

reviewed the

CRDR associated

with this event

and noted that it

addressed

the engineering

aspects

of the event,

but did not address

the

operations

aspects.

In response

to this comment,

engineering

issued

a memo to

all operations

managers,

informing them that taking the blowdown system out'f

service with the units at power could lead to a water

hammer event

when the

system is returned to service.

The inspector also learned that

a night order

had

been written to advise operations

personnel

of this event

and that initial

operator training includes

sessions

which focus

on identifying and preventing

water

hammer events.

This item is closed.

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PERSONS

CONTACTED

ATTACHMENT

1. 1

Arizona Public Service

Com an

J. Bailey, Assistant Vice'President;

Nuclear Engineering

P. Coffin, Engineer,

Nuclear Regulatory Affairs

E. Dutton, Supervisor, guality Control, Unit 2

A. Fakhar,

Manager, Site Mechanical

Engineering

R. Flood, Plant Manager,

Unit 2

D. Garchow, Director, Site Technical

Support

W. Ide, Plant Manager,

Unit

1

A. Krainik, Manager,

Nuclear Regulatory Affairs

D. Larkin, Senior Engineer,

Nuclear Regulatory Affairs

J.

Levine, Vice President,

Nuclear Production

D. Mauldin, Director, Site Maintenance

and

Modifi'cations'.

Russo,

Manager,

Maintenance

Nuclear Assurance

J. Scott, Assistant Plant Manager,

Unit 3

C.

Seaman,

Director, Nuclear Assurance

G. Shanker,

Department

Leader,

Engineering Nuclear Assurance

E. Simpson,

Vice President,

Nuclear Support

J. Velotta, Director, Training

P. Wiley, Manager,

Operations,

Unit 2

1.2

NRC Personnel

B. Olson, Project Inspector',

WCFO

1.3

Others

J. Draper, Site Representative,

Southern California Edison

B. Drost, Engineering .and Operations

Committee Alt., Salt River Project

F. Gowers, Site Representative,

El

Paso Electric

All personnel

listed were in attendance

at the exit meeting held with the

NRC

resident

inspectors

on June

15,

1994.

2

EXIT MEETING

An exit meeting

was conducted

on June

15,

1994.

inspectors

summarized

the scope

and findings of

acknowledged

the inspection findings documented

did not identify as proprietary any information

the inspectors.

During this meeting,

the

.

the report.

The licensee-

in this report.

The licensee

provided to, or reviewed by,

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