ML17300A885

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Insp Repts 50-528/87-10,50-529/87-11 & 50-530/87-12 on 870223-0404.Violations Noted:Failure to Remove Piece of Measuring & Test Equipment Overdue for Calibr from Svc & to Satisfy Tech Specs Re Pressurizer Heater Operability
ML17300A885
Person / Time
Site: Palo Verde  
Issue date: 05/15/1987
From: Ball J, Fiorelli G, Ivey K, Richards S, Sorensen C, Zimmerman R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML17300A883 List:
References
TASK-2.E.4.2, TASK-2.F.1, TASK-TM 50-528-87-10, 50-529-87-11, 50-530-87-12, GL-85-06, GL-85-22, GL-85-6, IEB-86-003, IEB-86-3, NUDOCS 8706050256
Download: ML17300A885 (51)


See also: IR 05000528/1987010

Text

U. S.

NUCLEAR REGULATORY CGYMISSION

REGION

V

Report Nos:

Docket Nos:

License

Nos:

Licensee:

Facilit

Name:

50-528/87-10,

50-529/87-11,

50-530/87-12

50-528, 50-529,

50-530

NPF-41,

NPF-51,

NPF-65

Arizona Nuclear

Power Project

P. 0.

Box 52034

Phoenix,

AZ. 85072-2034

Palo Verde Nuclear Generating Station Units 1,

2 5 3.

Ins ection Conducted:

February 23, through April 4, 1987.

Inspectocs:

Rl

R.

Zimme

, Senior

esi ent

nspector

J.

a

,

ident Inspector

/5 d'7

at

i ned

/s'7

at

gned

iore

,

es

ent

nspe tor

a

gne

Approved By:

K. Ivey

si ent Inspect r

orens,

rogect Insp

tor

S.

c

r s,

ie

,

ng

eering

ection

at

Si

ne

/s 8

Dat

igne

Mz~ gT

e

igned

Summary:

Ins ection

on Februar

23, throu

h A ril 4, 1987,

Re ort Nos.

50-52

-10

50-529

8 -11,

an

5 -530 8 -12

t

g

8706050256

870521

PDR

  • DOCK 05000528

6

PDR

Areas Ins ected:

Routine, onsite, regular

and backshift inspection

by

t e four resident inspectors,

and one regional inspector.

Areas

inspected

included: followup of previously identified items; review of

plant activities; plant tours; engineered

safety feature

system

walkdowns; surveillance test witnessing; plant maintenance; initial fuel

load witnessing;

preoperational

test results

review; overall startup test

program; operational staffing; quality assurance

for measuring

and test

equipment

(NIENTE); inoperable pressurizer

heater control switch;

pressurizer

level control problems; verification of containment

inte rit

eneric letter followup; TMI Action Plan Items; 50.55(e)

reports

(DERs); design

changes;

licensee

event report followup; and

periodic and special

reports

review.

Ouring this inspection the following Inspection

Procedures

were covered:

25401,

30702,

30703,

35744,

35750,

36301,

37301,

61715,

61720,

61726,

62703,

70322,

70324,

70326,

70532,

70534,

70537,

70539,

70548,

70554,

71302,

71707,

71710,

72400,

72500,

72524,

90712,

92700,

92701,

92703,

92719,

93702,

94300.

Results:

Of the 20 areas

inspected,

two violations were identified.

Failure to remove from service

a piece of measuring

and test equipment

which was overdue for calibration - paragraph

8; and fai lure to satisfy

a

Technical Specification associated

with pressurizer

heater operability-

paragraph

9.

DETAILS

Persons

Contacted:

The below listed technical

and supervisory

personnel

were

among

those contacted:

Arizona Nuclear

Power Pro ect

ANPP

"R. Adney

~J. Allen

  • L. Brown

R, Buckhalter

"J.

R.

Bynum

B. Cederquist

J.

Dennis

W.

Fernow

  • D. Gouge
  • J.

G.

Haynes

  • W.

E.

Ide

W.

Jump

J. Kirby

A. McCabe

0 ~ Nelson

  • R. Nelson

G. Perkins

~J. Pollard

F. Riedel

  • T. Shriver

L. Souza

"E.

E.

Van Brunt, Jr.

R. Younger

"0. Zeringue

Operations

Superintendent,

Unit 2

Operations

Manager

Radiation Protection

and Chemistry Manager

Outage

Management

Superintendent,

Unit 3

PVNGS Plant Manager

Chemical

Services

Manager

Operations

Supervisor,

Unit 1

Training Manager

Operations

Superintendent,

Unit 3

~ Vice President,

Nuclear Production

Corporate guality Assurance

Manager

Startup

Manager,

Unit 3

Project Transition Manager

Assistant Startup

Manager,

Unit 3

Operations

Security Manager

Maintenance

Manager

Radiological Services

Manager

Operations

Supervisor,

Unit 2

Operations

Supervisor,

Unit 3

Compliance

Manager

Assistant guality Assurance

Manager

Executive Vice President

Operations

Superintendent,

Unit 1

Technical

Support

Manager

The inspectors

also talked with other licensee

and contractor

personnel

during the course of the inspection.

"Attended the Exit Meeting on April 3, 1987.

Previousl

Identified Items

Unit 1

Closed

Enforcement

Item

528/85-26-04):

Overtime Controls.

The licensee

issued

Procedure

Change Notice No.

2 to procedure

10AC-OZZ07, "Overtime Limitations" on January

19, 1987.

This change

increased

the unit staff governed

by the overtime controls to

include engineering

personnel

involved in taking measurements

or

making physical

changes

or adjustments

to installed safety related

equipment.

This item is closed.

Unit 2

a.

Closed

Followu

Item

529/86-26-01:

Non-Class

Blowers

Coolin

Radiation Monitors.

This matter dealt with the

use of air blowers to cool radiation

monitors to extend the operating lives of the instruments.

New

circuit boards

which are rated for higher temperature

operation

have

been purchased

and are being installed in the Unit 2

Technical Specification effluent monitors.

Plans are'to

replace

the boards in similar radiation monitoring units in

both Units 1 and

3 in the near future.

This item is closed.

b.

Closed

Enforcement

Item

529/86-32-04):

Licensee

Event

Re ort

LER

Failed to Include Cause of Valve Failure.

The inspector

reviewed documentation

which supported

the

completion of actions

taken

by the licensee

in connection with

the referenced violation.

These actions

included the

inspection

and cleaning of mufflers on similar solenoid valve

mufflers as installed

on SGB-500/, training of craft personnel

on the need for thoroughly documenting work performed

and

observations

made,

and the issuance

of a supplement

to Unit 2

LER 86-46 describing the cause of the failure of valve

SGB-500(.

A modification package for the removal of the

mufflers has

been

issued for each of the three units.

The

actions are considered

consistent with the licensee's

response

to the violation.

This item is closed.

C.

Closed)

Followu

Item

529/86-32-06

Maintenance

and Testin

on Valve SGB-UV 222.

This matter is related to followup actions taken by the

licensee to confirm the cause for the dual position indication

related to valve

SGB-UV 222 during an actuation

on

September

22,

1986.

The inspector

observed

work 'documents

associated

with the reed switch adjustment

on the valve and the

successful

retest of the valve stroke

and position indication.

This item is closed.

d.

Closed

Followu

Item

529/86-32-07

Combustible

Gas

Prep erational

Test Problem.

This matter dealt with a licensee

commitment to conduct

training discussions

related to radiation controls with plant

personnel

as

a result of a radiation airborne incident which

occurred during the testing of the Unit 2 hydrogen-oxygen

monitor system.

Discussions with several

radiation staff

members

and maintenance

personnel

by the inspector

determined

that discussions

dealing with radiation controls

have

been

conducted

since the incident.

Several

such training sessions

were conducted prior to the Unit 2 extended

maintenance

outage.

Plans

are to continue these

discussions

as part of the "equality

Talk" sessions

held routinely by the plant staff.

This item is

cl osed.

Unit 3

a.

(Closed

Followu

Item (530/86-03-03

Redundant

Class lE

Racewa

Mounted on a

Common

Su

ort.

b.

This item dealt with a concern raised during the

NRC

headquarters

Construction

Assessment

Team

(CAT) inspection of

Unit 3 conducted

in January,

1986 relating to the mounting of

class

1E raceways

of redundant trains

on a

common support,

and

a perception that

a single failure could possibly

effect more

than

one train of equipment required for safe

shutdown

adversely.

Engineering evaluations

including walkdowns of

plant areas

were performed

by the licensee to assure

that

potential

hazards either by fire or high energy missiles

were

accounted for in the plant design.

A review of the licensee's

evaluations

and confirmatory walkthroughs of plant areas

by the

inspector identified no discrepancies

in the licensee's

analyses.

Based

on this review, the inspector

concluded that

it appears

the licensee

has adequately

assessed

the impact of a

single failure of a raceway support

on redundant trains of

safety-related

equipment.

This item is closed.

Closed

Fol 1owu

Item

530/86-03-08:

Seismic

ualification of

Diesel Generator

Control Cabinets.

This item dealt with a concern raised during the

NRC

headquarters

CAT inspection of Unit 3 conducted in January,

1986, relating to the seismic qualification records for the

class

1E diesel

generator control cabinets.

In particular,

certain documentation

was not found which was

needed

in order

to adequately

determine the resolution of test discrepancies

found during the initial seismic test.

At the time of the

inspection,

the licensee

committed to update the qualification

records to reflect later retest results.

During this

inspection,

the inspector

reviewed documentation

of the retests

.

that were conducted

and concluded the licensee

had adequately

addressed

the original test discrepancies.

This item is

closed.

C.

Closed

Followu

Item

530/86-03-14

HVAC Exhaust For

Installation Acce tance Criteria.

This item dealt with a concern raised during the

NRC .

headquarters

CAT inspection of Unit 3 conducted in January,

1986, relating to a lack of clear acceptance criteria for the

tightening of the nuts anchoring the diesel

generator

exhaust

fans to the Diesel

Generator

Building on fabreeker

pads

using

embedded

anchor bolts.

This concern

was documented

by the

licensee

on Corrective Action Report

(CAR) S-86-13.

During

this inspection,

the inspector

reviewed the response

given to

the

CAR and the actions

taken

by the licensee

which included

revision to construction specifications to clearly define the

acceptance criteria for these installations

and confirmation

that the fans installed in all three units met the criteria.

Based

on the action taken

by the licensee

and the inspector's

review, this item is closed.

Closed)

Followu

Item

530/86-03-21:

Thermal

Loadin

of

Structural Steel.

This item dealt with questions

raised during the

NRC

headquarter's

CAT inspection of Unit 3 conducted

in January

1986

as to whether thermal effects

on seismic category I steel

structures

had been adequately

considered

in the plant design.

This matter was referred to

NRR for resolution.

In Supplement

No.

10 of NUREG-0857, "Safety Evaluation Report Related to

Operation of Palo Verde Units 1, 2,

and 3",

NRR documented its

conclusion

based

on additional information provided by the

licensee that the licensee's

approach

to handling thermal

effects

was acceptable.

Based

on the conclusion

reached

by

NRR, this item is closed.

Closed

Followu

Item

530/86-03-22

Desi

n Chan

e

Documentation.

The original concern involved several

instances

where

a design

change

was

made

and referenced

to a specific design

document

without changes

being made to other applicable design

documents.

Also involved were documentation

errors

on certain

Field Change

Requests

(FCRs).

The licensee

requested

Bechtel, in writing, to address

these

concerns.

Bechtel

responded

by stating that the problems

identified were strictly associated

with specific valves that

were procured

under the

Non Traditional Acquisition program.

This program allowed

a quicker acquisition time because

components

were acquired

from nuclear power plants that had

been cancelled

and therefore,

components

acquired

under this

program

had already

been certified.

Approximately 63 valves were identified in Unit 3 which were

acquired in this manner.

The valves were inspected

and design

documents

were reviewed to ensure

conformance to the as-built

condition.

Where design

documents

were not in agreement with

the as-built,

changes

were issued.

Also, the documentation

errors associated

with the

FCRs were

determined to be minor in nature.

Since the only way to change

an

FCR is to issue

a new one to supercede

the old one,

a

decision

was

made not to issue

new FCRs.

The inspector

found this response

to be acceptable

and this

item is closed.

(Closed

Followu

Item

530/86-20-01):

Valve 0 erator

Dama

e

Followin

Primar

H drostatic Testin

.

This item concerned

the affects of a solid plant transient

event which occurred

subsequent

to the reactor

coolant system

initial, primary hydrostatic test

when

a reactor coolant

pump

was started

during the system

cooldown.

During this event,

the

valve motor operator for an isolation valve located

on one of

the two shutdown cooling lines was

damaged.

At the time of the

event,

the cause of the

damage

sustained

by the valve operator

had not been completely evaluated.

During this inspection,

the

inspector

reviewed the actions

taken

by the licensee

in

determining the root cause for the valve damage

and what if any

other

damage

may have

been sustained

by the piping system.

Further,

the inspector's

review considered

what generic

implications this event might have to similar installations.

The licensee,

based

on

a detailed examination of the valve

operator

and

a review of installation records for the affected

valve, concluded that the operator-to-valve

yoke bolts/nuts

had

been under-torqued.

The loose bolting is considered

to have

left the valve in a weakened condition such that the piping

vibration that was experienced

during the starting of the

reactor coolant

pump shook the valve operator to a degree that

it sustained

damage that would not normally be expected to

occur during such

an upset condition.

The licensee

performed

a

detailed walkdown of the piping system.

Ho other discrepancies

were noted.

Subsequent

inspection of 100 other valves

identified some other instances

in which, when retorqued,

slight bolt movement occurred;

however, in most cases

no

movement

was found.

The licensee

concluded that slight

movement

was not necessarily

indicative of under-torquing

during initial installation.

The licensee

concluded in Startup

Field Report SI-171 that based

on sample size the failure to

properly torque the valve bolting did not appear to be

a

generic

problem or to have affected the operability of other

valve installations.

Items identified by the licensee

as not

meeting specific torque requirements

have

been

reworked.

Based

on the corrective actions

taken by the licensee

and the

inspector's

review, this item is closed.

(Closed

Followu

Item (530/86-26-01:

Si nificant

E ui ment

Problems Identified Durin

Hot Functional Testin

.

This item related to concerns

by the inspector associated

with

several

equipment

problems that developed during Hot Functional

Testing.

These

included

a problem with a leaking letdown heat

exchanger

nozzle;

a steam generator

instrument nozzle which

also developed

a leak; the unanticipated

opening of a main

steam isolation valve (MSIV); and,

problems with the vital AC

inverters.

During this inspection,

the inspector

reviewed the

actions

taken

by the licensee to correct and define the root

cause for these

problems.

Both the leaking nozzle

on the

letdown heat exchanger

and

on the steam generator

were repaired

and

a root cause

analysis

performed

by the licensee.

The

analysis of the leaking heat exchanger

nozzle indicated that

fatigue and an inadequate

weld design contributed to the

failure while the failure of the steam generator

nozzle

has

been attributed to damage

sustained

during construction

activities.

Problems with the vital

AC inverter were corrected

by the licensee

by a modification to the inverter circuitry

which lessened its sensitivity to momentary voltage

perturbations

on the

DC bus.

Troubleshooting of the MSIV by the licensee;

however, did not

determine

what caused

the unanticipated

opening of the valve.

By letter dated March, 20,

1987, the licensee

committed to the

NRC to reperform troubleshooting efforts during post core hot

functional testing in an effort to duplicate the previous

event.

The inspector will continue to monitor the licensee's

efforts in this event.

Based

on the inspector's

review of

actions taken

by the licensee

and the commitments

made, this

item is closed.

3.

Review of Plant Activities

a.

Unit 1

Unit 1 was restarted

and entered

Mode 1 on March 4, 1987,

ending

an unscheduled

45 day outage for steam generator

tube

plugging.

Power was reduced to Mode

2 on March

5 to repair

valve and hanger

damage

which resulted

from a water

hammer

in

the heater drain tank high level

dump lines.

The unit entered

Mode 1 again

on March 6 and was increasing

power when

a turbine

trip was received

on high moisture separator

reheater

(MSR)

water level.

Work on the

MSR level control

was completed

and

power raised to 100K on March 7.

For the period from March 7

to March 27, reactor

power was increased

and decreased

as

necessary

for condenser

tube plugging,

steam generator water

chemistry problems,

and condensate

demineralizer

problems.

Full

power operation

was maintained

from March 27 to the end of this

reporting period.

b.

Unit 2

C.

Unit 2 restarted

from a 59 day scheduled,

maintenance

outage

on

March 9, 1987.

Two outages of short duration were required

on

March 11 and March 17 to locate

and plug main condenser

tube

leaks.

The plant was restarted

on March 20 and power raised to

50K.

Loss of a heater drain

pump and erratic operation of the

pressurizer

level instrumentation

(paragraph

10) resulted in

50K power operation until March 28 when the pressurizer

level

control instrumentation

was repaired.

A short period of

operation at 85K was required

on March 30 due to an inoperable

control element

assembly calculator.

Following repairs,

power

level was raised to lOOX and full power operation

was continued

through the end of the reporting period.

Unit 3

During this report period,

the licensee

performed final reviews

of system construction completion

and preoperational

testing,

~

and completed surveillance testing of systems

required for

initial entry into Mode 6.

On March 25, 1987, the licensee

was

issued

a low power operating license permitting the licensee

to

commence

loading fuel.

On April 4, 1987,

the licensee

entered

Mode

6 with placement of the first fuel assembly in the reactor

vessel.

During this report period, repairs to the "B" Diesel

Generator

engine block and crankcase,

which were

damaged during

preoperational

testing,

were also completed

and reassembly

of

the diesel

engine

begun.

d.

Plant Tours

The following plant areas

at Units 1,

2 and

3 were toured by

the inspector during the course of the inspection:

Auxiliary Building

Containment Building

Control

Complex Building

Diesel Generator Building

Radwaste

Building

Technical

Support Center

Turbine Building

Yard Area and Perimeter

The following areas

were observed

during the tours:

1.

0 eratin

Lo s and Records

Records

were reviewed against

Technical Specification

and administrative control pro-

cedure

requirements.

The inspector

reviewed several

recent night orders at Unit

2 which were considered

to be bordering

on providing

direction to the operators

by a means for which the

procedure

change

process

was intended.

The inspector

discussed

the matter with licensee

management

and

concluded that additional administrative direction was

warranted

to ensure that night orders

were not used in

place of initiating procedural

changes.

The licensee

acknowledged

the inspector's

comments

and revised

paragraph

10.5 of administrative procedure

40AC-9ZZ02,

"Conduct of Shift Operations",

shortly after the

completion of the inspection period, to clearly state that

night orders

are not to be used to make changes

to safety

related procedures.

Night orders will continue to be

reviewed

as part of the routine inspection

program;

2.

Monitorin

Instrumentation

Process

instruments

were

observed for correlation

between

channels

and for con-

formance with Technical Specification requirements.

3.

observed for conformance with 10 CFR 50.54. (k), Technical.

Specifications,

and administrative procedures.

E ui ment Lineu

s

Valve and electrical

breakers

were

verified to be in the position or condition required

by

Technical Specifications

and Administrative procedures

for

the applicable plant mode.

This verification included

routine control board indication reviews

and conduct of

partial

system lineups.

5.

E ui ment Ta

in

Selected

equipment, for which tagging

requests

had been initiated,

was observed

to verify that

tags were in place

and the equipment

was in the condition

specified.

6.

General

Plant

E ui ment Conditions

Plant equipment

was

observed for indications of system

leakage,

improper

lubrication, or other conditions that would prevent the

associated

system

from fulfillingtheir functional

requirements.

7.

Fire Protection

Fire fighting equipment

and controls were

observed for conformance with Technical Specifications

and

admi nistrati ve procedures.

8.

for conformance with Technical Specifications

and admin-

istrative control procedures.

9.

10.

~Secorit

Activities observed for conformance with

regulatory requirements,

implementation of the site

security plan,

and administrative procedures,

included

vehicle and personnel

access,

and protected

and vital area

integrity.

Plant Housekee

in

Plant conditions

and material/-

equipment storage

were observed to determine the general

state of cleanliness

and housekeeping.

Housekeeping

in

the radiologically controlled area

was evaluated with

respect

to controlling the spread of surface

and airborne

contamination.

Radiation Protection Controls

Areas observed

included

control point operation,

records of licensee's

surveys

within the radiological controlled areas,

posting of

radiation

and high radiation areas,

compliance with

Radiation

Exposure

Permits,

personnel

monitoring devices

being properly worn, and personnel

frisking practices.

No violations of NRC requirements

or deviations

were identified.

4.

En ineered Safet

Feature

S stem Malk Gown - Units 1

2 and

3

Selected

engineered

safety feature

systems

(and systems

important to

safety) were walked

down by the inspector to confirm that the

systems

were aligned in accordance

with plant procedures.

During

the walkdown of the systems,

items

such

as hangers,

supports,

electrical cabinets,

and cables

were inspected

to determine that

they were operable,

and in a condition to perform their required

functions.

The inspector also verified that the system valves were

in the required position and locked as appropriate.

The local

and

remote position indication and controls were also confirmed to be in

the required position and operable.

Unit 1

Portions of the following systems

were walked

down on the indicated

date.

~Setem

Auxiliary Feedwater

System,

Trains "A" and "B"

Date

March 20

Containment

Spray System,

Trains "A" and "B"

Diesel Generator,

Trains "A" and "B"

February

23,

March 18

March

5

Essential

Cooling Mater System,

Trains "A" and "B"

March 18

High Pressure

Safety Injection System,

Trains "A" and B"

March 18

Supplemental

Protective

System

125V

DC Electrical Distribution,

Channels

"A" and "B"

April 2

March

5

Fire Suppression

System (Fire Pumps,

Supply and Discharge Valving)

February

25

Unit 2

Portions of the following systems

were walked down on the indicated

dates.

~Setem

Fire Suppression

System (Fire Pumps,

Supply and Discharge Valving)

Date

February

25

Safety Injection Tanks

March

6

10

Essential

Spray Ponds,

Trains

"A" and "B"

Auxiliary Feedwater

System,

Train "8"

March

13

March 20

Control

Room Emergency Ventilation

System, Trains "A" and "B"

125V

DC Electrical Distribution,

Channel

"A"

March 24

March 31

Unit 3

Portions of the following systems

were walked

down on the indicated

dates.

~Ss ten

Diesel Generator

System - Train "A"

125V

DC Electrical Distr ibution Channel

IIAII and

IIC II

Date

April 1

March 30

No violations of NRC requirements

or deviations

were identified.

5.

Surveillance Test Witnessin

- Units 1,

2 and

3

'a ~

Surveillance tests

required to be performed

by the Technical

Specifications

(TS) were reviewed

on a sampling basis to verify

that:

1) the surveillance tests

were correctly included

on the

facility schedule;

2)

a technically adequate

procedure

existed

for performance of the surveillance tests;

3) the surveillance

tests

had been

performed at the frequency specified in the TS;

and 4) test results satisfied

acceptance

criteria or were

properly dispositioned.

b.

Portions of the following surveillance tests

by the inspector

on the dates

shown:

Unit I

were witnessed

Procedure

36ST-1SE06

73ST-9CL03

41ST-1DG01

Descri tion

Log Power Functional Test

Containment Airlock Seal

Leak Test

Diesel Generator

"A" Test

4.8.1.1.2.A

Dates

Performed

February

26

February

27

February

27

41ST-1SG01

Main Steam Line Isolation

Val ves Surveillance 4.7.1.5

March 3

36ST-9SB02

72ST-9RX02

PPS Bistable Trip Units

Functional Test

Moderator Temperature

Coefficient At Power

March 4,

31

April 1

March 19

36ST-9SA02

Unit 2

ESFAS Train

B Subgroup

Relay

March 21

Monthly Functional

Test

Procedure

36ST-2SE03

42ST-CH06

36ST-9SB01

73ST-9CL03

77ST-9SE09

Unit 3

Procedure

32ST"9PK04

31ST" 9DG01

43ST-3DG01

Descri tion

Excore Safety Linear Channel

quarterly Calibration

Charging

Pump Operability

Test

CEA Reed Switch Functional

Test

Containment Airlock Seal

Leak Test

CPC Channel

"C" Functional

Test

Descri tion

60-Month Surveillance of

Station Batteries for

3E PKC-F13 - Channel

"C"

Diesel

Engine Inspection

- Train "A"

31-Day. Surveillance of

Diesel Generator - Train

I IAlI

Dates

Performed

February

24

February

24

February

26

March 3

March 31

Dates

Performed

March 2

Mar ch 23

March 24

43ST"3CH02

Boron Injection Flowpaths

March 24,

28

- Shutdown

32ST-9PK02

32ST-9PK03

92-Day Surveillance of

Station Batteries for

3E PKC-F13 - Channel

"C"

18-Month Surveillance of

Station Batteries for

3E PKC-F13 - Channel

"C"

March 26

March 27

12

73ST-9FH01

Refuel ing Machine

Load

Test

March

27'o

violations of NRC requirements

or deviations

were identified.

6.

Plant Maintenance - Unit 1

2 and

3

a 0

During the inspection period, the inspector

observed

and re-

viewed documentation

associated

with maintenance

and problem

investigation activities to verify compliance with regulatory

requirements,

compliance with administrative

and maintenance

procedures,

required

QA/QC involvement, proper

use of safety

tags,

proper equipment alignment

and

use of jumpers,

personnel

qualifications,

and proper retesting.

The inspector verified.

reportability for these activities was correct.

b.

The inspector witnessed portions of the

activities:

following maintenance

Unit 1

o

Monthly Auxiliary Relay Cabinet

Inspection

o

Replacement

of Fuel

Lines on the

"A" Diesel Generator

Dates

Performed

February

26

February

26,

27

o

Clean

and Inspect

Fuses

in the

Plant Protection

System

(PPS)

Cabinets

February

27

o

Troubleshoot

Heater Drain Tank

High Level

Dump Valve

March 5

o

Rework of Damaged

Pipe Supports

on Heater Drain Tank Lines

March

5

o

Instrument

Loop Check of

Engineered

Safety Feature

(ESF) Equipment

Rooms

Smoke

Exhaust

System

March 20

o

Troubleshooting of Emergency

Response, Facility Data Acquisition

and Display System

(ERFDADS)

Problems

March 26

o

Troubleshoot

and Rework/Replace

Problem with Control

Room

Annunciator Window 1B15D

March 31

o

Replace

Various Westinghouse

"SCPB" Circuit Breakers

March 31

0

13

Unit 2

Deecri tion

Dates

Performed

o

Replacement of the Outer

140'ontainment

Airlock Door Seal

March

3

o

Replacement

of Containment

Spray Injection Valve

UV 572

o

Installation of a High

Temperature Circuit Board

Into the

RU 31 Radiation Monitor

March

5

April 1

No violations of NRC requirements

or deviations

were identified.

Disablin

of En ineered Safet

Feature - Unit 1

On January

20, 1987, Unit 1 was in Mode 4, proceeding to cold

shutdown following the identification of a tube leak in Steam

Generator

(S/G) No. 1.

The faulted steam generator

was isolated

and

the cooldown was accomplished

through

S/G No.

2 to the main

condenser.

Night orders

were issued to maintain forced circulation

with reactor coolant

pumps until the S/G No.

1 metal temperature

dropped to about

90 degrees

F.

Although permitted by procedure,

in

the past forced circulation had not normally been maintained this

far into the cooldown.

Mith the average

reactor coolant system

temperature

at about

250 degrees

F and steam generator

pressure

at

25 psia, pretrips were received for all four channels

of main steam

isolation system

(MSIS) actuation.

The cause of the pretrips

was

the proximity of the actual

steam generator

pressure

to the pretrip

setpoint,

aggravated

by the maintenance

of forced circulation

through the steam generators.

The MSIS setpoint is variable,

allowing manual control over the setpoint to permit a controlled

plant shutdown,

including depressurization

of the steam generators.

The variable setpoint is reduced in 200 psia increments until

essentially

a zero setpoint is reached,

discounting instrument

inaccuracies

and drift.

Following receipt of the MSIS pretrips,

the

operating

crew evaluated

the condition and elected to simulate

signals to the steam generator

pressure

bistables

to prevent

a

possible

MSIS as secondary

pressure

continued to drop.

Technical Specification (TS) 3.0.3

was voluntarily entered

since the

MSIS

safety feature

was required operable

by TS 3.3.2 until Mode 5 entry.

Operations

supervision,

above the shift supervisor,

was not

consulted

regarding the decision to simulate bistable inputs

and to

voluntarily enter into TS 3.0.3.

ANPP procedure

36MT-9SB03,

"PPS

Bistable Input Simulation" was

used to input the simulated signals;

however, the procedure

stated,

in paragraph

1. 1.2, that only

bistables

not required

by TS 3.3.2 for the plant mode at that time

may receive simulated signals to prevent actuation.

The

significance of this issue is still under evaluation

by the staff

and will be addressed

in future correspondence.

Thus, the issue is

unr esol ved (528/87-10-01).

1

14

Following the

NRC review of this event,

as

documented

in Licensee

Event Report 87-07,

a confirmatory action letter (CAL) was

transmitted to the licensee

on March 6, 1987 to address

the Region

V

concern regarding the method by which TS 3.0.3 was entered.

The

CAL

addressed

the following actions

taken or planned

by the licensee:

o

A planned revision to the appropriate administrative

procedure

to preclude intentionally entering

TS 3.0.3 unless justified by

emergency conditions or as otherwise authorized

by approved

procedure es.

o

The need to promptly ensure plant personnel

including

supervision, fully understand

the licensee's

policy for

voluntary entry into TS 3.0.3.

Additionally, a meeting

was held in the

NRC Region

V Office on March

ll, 1987, at which time the above event

was reviewed with

appropriate

licensee

personnel

in detail.

The meeting included

discussion of the following issues:

o

Had the night order been

supplemented

with a preshift briefing

to explore possible

problems which might be encountered

during

the cooldown, the potential for a MSIS actuation

may have

been

foreseen.

This is accented

by the fact that a forced

circulation cooldown as addressed

in the night order

had not

previously

been performed.

o

Plant personnel

should fully understand

that when unusual

conditions arise they should stop the evolution in progress, if

practicable,

until the situation is evaluated

by higher levels

of supervision.

o

The event

was

due in part to a plant design conflict with

Technical Specifications.

Technical .Specification 3.0.3

was

used

as

an operational

convenience

to temporarily deal with the

conf 1 ict.

The inspectors

reviewed the technical details of the event to

ascertain

whether the plant had been placed in an unsafe condition

or whether

any technical specification

requirements

had been

violated.

The following observations

were

made:

At the time of the event,

the reactor

was completely shutdown,

with all control rods inserted,

and the reactor coolant system

borated to cold shutdown conditions.

The automatic

MSIS feature,

on low steam line pressure

is

provided primarily to terminate or mitigate

a reactivity

addition accident, caused

by a main steam line break

and the

resulting primary cooldown.

At the time of the event,

the ¹1

Steam Generator

was already isolated.

The ¹2 Steam Generator

pressure

was approximately

25 psia.

The main steam line design

operating pressure

is approximately

1000 psia, therefore the

15

probability of a steam line break at 25 psia appears

to be

extremely remote.

With the reactor coolant system borated to cold shutdown

conditions,

the reactivity addition resulting from an

uncontrolled

cooldown would not result in a restart accident.

Water injection capability was available to rapidly recover

from any reactor coolant system contraction resulting from a

cooldown.

A review of other pressurized

water reactor

technical

specifications

(San Onofre, Oiablo Canyon, Trojan) indicates

that similar MSIS features

based

on low system line pressure

are not required in mode 4.

Palo Verde technical specification limiting condition for

operation

(LCO) 3.0.3,

which was intentionally entered

when the

LCO governing the

MSIS feature

was

no longer met, requires that

action

be taken within one hour to place the unit in a cold

shutdown condition (Mode 5), within the subsequent

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

At the time of the event,

the licensee

was already preparing to

enter

Mode 5,

and did enter

Mode 5 one hour and eighteen

minutes later.

Based

on the above,

the inspectors

concluded that the specific event

had

no direct safety significance

and that no technical

specification violation had occurred.

However, the inspectors

maintained that this event was very significant from the aspect that

a required engineered

safety feature

was disabled without

appropriate

management

oversight

and procedural

control.

In followup of the

CAL, the inspector

reviewed the licensee's

revision to ANPP procedure

40AC-9ZZ02, "Conduct of Shift Operation",

procedure

change notice

(PCN)

No. 8, which stated that voluntary

entry into TS 3.0.3 is prohibited unless justified by an emergency

condition or as authorized

by approved procedures.

The inspector

also reviewed training records

associated

with the licensee's

policy

regarding

TS 3.0.3 voluntary entry,

as well as providing personnel

direction to stop the performance of an activity and contact

supervision

when problems arise.

The inspector

s review of training

records

was ongoing at the conclusion of the inspection period.

This item (528/87-10-02) will remain

open pending 1) completion of

the training records

review by the inspector,

and 2) followup of the

licensee's

consideration

of the remaining potentially generic

issues

discussed

above

and in the

NRC letter

dated

March 13,

1987 from Mr.

J. Martin (NRC) to E.

Van Brunt, Jr.,

(ANPP) dealing with:

o

The benefit of preevolution briefings for new,

unusual

or

complex evolutions;

o

Whether additional conflicts exist between

aspects

of the plant

design

and Technical Specification;

and,

16

o

Whether provisions of the Technical Specifications

are being

implemented in a manner other than originally intended.

Calibration of Measurin

and Test

E ui ment - Unit 1

On March 31,

1987, during a tour of the Fuel Building, the inspector

noted that flowmeter EG-4092 (Brooks Rotometer)

had

a calibration

due date of March 13,

1987.

This flowmeter

was being used

on

a grab

sample cart which was connected to radiation monitor RU-145 (Fuel

Building Exhaust)

~

Further investigation revealed that RU-145 had

been inoperable

since

March 20,

1987 and the grab samples

were being

taken to comply with the actions of Technical Specification

(TS)

Limiting Condition for Operation

(LCO) No. 3.3.3.9.

The inspector

discussed this item with M&TE personnel

and reviewed calibration

documentation

to verify that the calibration due date

was March 13,

1987.

The flowmeter was

on a six month calibration frequency

and

was last calibrated

on September

8, 1986.

Procedure

34AC-9ZZ07,

"M&TE User's Administrative Requirements"

defines

M&TE that is overdue for calibration

as nonconforming

M&TE.

The responsibility for ensuring that

M&TE has not exceeded its

calibration

due date lies with the user.

The segregation

and

tagging out-of-service of nonconforming

M&TE is the responsibility

of the user

and the

M&TE custodian.

The failure to identify,

segregate,

and tag out-of-service

nonconforming

M&TE is contrary to

TS 6.8. 1 and the above administrative procedure,

and is considered

a

violation (528/87-10-03).

Ino erable Pressurizer

Heater Control Switch - Unit 2

At 5:00

PM on March 20, the operating staff determined that Control

Room switch HS-100, which is used to energize

a bank of class

1E

powered

backup pressurizer

heaters,

was inoperable.

The staff

confirmed that the breaker could be closed locally and consequently

the heater

bank could be energized.

The hand switch for the other

heater

bank was operable.

The staff believed that this satisfied

the

LCO in paragraph

3.4.3. 1 of the Technical Specifications

which

required at least

two groups of pressurizer

heaters

capable of being

powered from Class

1E buses.

The staff was

unaware of the

surveillance

requirement in paragraph

4.4.3. 1.3 of the Technical

Specifications

which required

an ability to connect the heaters

to

their respective

buses

manually from the Control

Room, until it was

questioned

by the inspector

on March 27.

A review of the matter

revealed

the Control

Room switch to be inoperable until 3:00

PM on

March 24,

a period of 94 hours0.00109 days <br />0.0261 hours <br />1.554233e-4 weeks <br />3.5767e-5 months <br />.

The unit remained in Mode 1 during

this time.

The action statement

associated

with the referenced

LCO

requires

the heater

bank (includes switch control) to be restored to

an operable

status within 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or the unit must be placed in

Mode

3 in the following six hours.

Exceeding the specified

Technical Specification time interval is considered

a violation of

the Technical Specification operability requirement

(529/87-11-01).

Pressurizer

Level Control - Unit 2

17

Following plant startup

on March 9, plant operators

experienced

erratic operation

on both

110X and

110Y pressurizer

level control

channels.

The control

system

had been recalibrated

during the

recent extended

maintenance

outage

and the initial rationale for the

erratic operation

was attributed to the

need for system tuning

following the outage work.

When system control adjustments

were not

successful,

investigative efforts were initiated to determine what

conditions could be contributing to the sluggish

response

of level

control.

Several

tests

were conducted

wherein reactor pressure

was increased

about

50 psig above

normal over varying periods of time.

Level

response

to the pressure

increase

on both channels

were comparable,

but increasingly less

responsive

when the time duration during which

reactor pressure

was increased

was shortened.

Following

confirmation that steady level control

was acceptable

but level

control during transient conditions

was not, channel

110Y was

declared

inoperable for failure to meet Technical Specifications 3.3.3.5

and 3.3.3.6,

remote

shutdown

and post accident monitoring

instrumentation,

respectively.

Channel

110X had been declared

inoperable previously,

when its level transmitter

was replaced.

With both channels

inoperable,

the most limiting action statement

associated

with the above

LCOs required returning one of the two

channels

to an operable

status within 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br />.

The control response

during the pressure

increase tests

suggested

that the sensing lines, which contained

7/32" orifices, could be

partially plugged.

Both sensing lines were flushed, following which

both channel

responses

returned to normal.

Ouring the flushing of

Channel

110Y, material which was black in color, magnetic

and

resembled

magnetite,

was observed to discharge

from the line.

Following completion of the surveillance tests

on both Channels

110X

and 110Y, each of the pressurizer

level channels

was returned to an

operable condition prior to exceeding

the Technical Specification

action statements

of 48 hours5.555556e-4 days <br />0.0133 hours <br />7.936508e-5 weeks <br />1.8264e-5 months <br /> for two inoperable

channels

and seven

days for one inoperable

channel.

Both level channels

have

been operating normally since the flushing

of the sensing lines.

The licensee's

actions in this matter are still under review by the

NRC and this item will remain

open until the review is completed

(529/87-11"02).

No violations of NRC requirements

or deviations

were identified.

Transient

Loadin

Considerations

- Unit 1

On March 20, 1987, during a general

tour of Unit 1, the inspector

noted that scaffolding had been erected

around class

1E cable

raceways

in the Train "B" switchgear

room.

Also, two boards

(approximately

3 feet square)

were lying on the cable

raceway

and

were tied to the scaffolding.

This scaffolding was erected to

18

support

an instrument

'loop check

on the

ESF equipment

rooms

smoke

exhaust

dampers

(W.O. 206700).

Discussion

and review of this situation with licensee

work control

and scaffolding personnel

revealed that the boards

were to be used

by mai'ntenance

personnel

to stand

on and access

a damper located

over the cable tray.

The inspector

expressed

a concern

over the

additional

loading on the raceway supports after noting that

a

safety analysis

accounting for the transient

loading provided by the

scaffolding and boards

had not been performed.

The licensee

has previously performed

a bounding calculation to

account for the transient

use of lead blanketing

on piping.

However,

no such calculation

had been performed for cable

raceway supports.

The licensee

committed to complete

a bounding calculation for the

loading effect on the worst case

cable support

by April 24,

1987

'urther,

the licensee

has also committed to evaluate

the need for

bounding calculations for other transient

loading situations.

This item will remain unresolved

pending the completion of the

licensee's

calculations

and the correlation to the specific instance

identified (528/87-10-04).

Verification of Containment Inte rit - Units 1 and

2

Prior to entry into Mode 4 on March 1 and 4, 1987, respectively,

the

inspector verified that the licensee

had established

containment

integrity.

For each unit, the inspector:

o

Witnessed the satisfactory

completion of Procedure

73ST-9CL03,

"Airlock Local

Leak Rate Test".

I

o

Verified, through field observations,

that all mechanical

barriers

and isolation valves associated

with ten containment

penetrations

were in their proper position.

o

Verified the operability of the Containment

Spray system

by a

field walkdown of system

components

and

a review of the

system's

Control

Room indications.

No violations of NRC requirements

or deviations

were identified.

Initial Fuel

Load Witnessin

- Unit 3

The licensee

entered

Mode

6 on April 4,

1987.

The initial fuel

loading was witnessed

by the inspector to verify that the activities

were performed in conformance with Technical Specifications.

The

inspector

observed fuel loading activities from the spent fuel

machine in the Fuel Building; refueling machine in Containment;

and,

the Control

Room.

The activities were compared to the requirements

of procedure

73IC-3RNOl, "Initial Fuel

Load" and to the Technical

Specifications.

The inspector verified that:

c

V'

19

o

On a sampling basis,

the prerequisite

Mode

6 and the "At All

Times" Technical Specifications

had been completed prior to the

start of fuel handling.

o

The crew complement

was staffed with qualified personnel

in

accordance

with Technical Specifications.

o

The senior reactor operator in charge of fuel handling was in

constant

communication with the Control

Room.

o

The inverse multiplication plots were being calculated

and

plotted by the reactor engineering

group.

o

The boron concentrations

in the reactor coolant system

and

Refueling Water Storage

Tank were within limits.

o

A fuel management

control board

was set

up to identify the

location of each fuel assembly

as it was

moved from the Fuel

Building to the reactor vessel.

The test director was observed

to be supervising

the fuel movements

from the Control

Room

location.

o

Initial fuel load procedure

changes

were implemented in

accordance

with administrative controls.

No violations of NRC requirements

or deviations

were identified.

14.

Prep erational

Test Results

Review - Unit 3

The inspector

reviewed the completed test procedures

and test result

reports for the following system preoperational

tests:

Procedure

90HF"3ZZ01

91P E-3DG01

91PE" 3EC01

91P E-3EW01

91PE" 3SP01

91P E-3SGOl

91P E-3SG04

91HF-3SG01

91HF" 3RC02

92PE-3SE01,

02,

03, 04,

05 and

06

92PE-3SF01,

02

92HF-3SF01

93PE-3PE01

93P E"3SA01

Precore

Hot Functional Testing

Diesel Generator

System

Essential

Chilled Water System

Essential

Cooling Water System

Essential

Spray

Pond System

Main Steam Isolation Valves and Bypass

Valves

Steam Generator Isolations

Main Steam Isolation Valves and Bypass

Valves

Hot Functional Test

Pressurizer

Performance

Excore Nuclear Instrumentation

Feedwater

Control

System

Precore

CEDM Performance

Diesel Generator Electrical Test

Integrated Test of Engineered

Safety Features

The inspector verified that activities such

as test data

acquisition, test exception resolution, test report issuance,

test

modifications

and acceptance criteria verification had been

0

20

accomplished

in accordance

with the licensee's

FSAR commitments

and

administrative controls.

No violations of NRC requirements

or deviations

were identified.

Overall Startu

Test Pro

ram - Unit 3

The inspector

reviewed the post core testing program for Unit 3.

The

administrative controls

such

as test conduct, test procedure

review

and approval, test results

review and approval,

document control,

test program organizational

structure

and administration,

and use of

measurement

and test equipment,

were found to be essentially

the

same

as those

used in Units 1 and 2.

Revisions to the procedures

were found to be limited to minor changes

which did not affect

FSAR

commitments.

Test controlling procedures

associated

with initial fuel load,

initial criticality, post core hot functional testing

and power

ascension

testing are expected to be the

same

as those

used in

Unit 2.

The licensee

has prepared

FSAR changes

which would

eliminate certain testing in Unit 3 based

on successful

tests

in

Units 1 and 2.

This includes elimination of a loss of offsite power

test,

atmospheric

dump valve/steam

bypass

valve capacity tests

and

Core Protection Calculator/Core

Operating Limit Supervisory

System

verification tests at

20% and

80%.

The licensee is also seeking

relief with regard to requirements for establishing equilibrium

xenon conditions prior to physics testing.

The licensee

does plan

on conducting

a remote

shutdown test from outside the Control

Room

at the

20% plateau.

Specific test procedures

for Unit 3 shall

be

reviewed by the inspector

as they are

made available prior to test

conduct;

No violations of NRC requirements

or deviations

were identified.

Desi

n Chan

es - Unit 3

The inspector selected

a representative

sampling of design

change

packages

(DCPs) for Unit 3.

The inspector

chose

DCPs from the

mechanical, electrical,

and

I&C groups.

The inspector

reviewed the

DCPs to ensure that the changes

were properly reviewed

and approved;

revisions

were properly reviewed

and approved,

acceptance

tests

were

performed

as required;

and,

independent

design verifications were

performed

as required.

No violations or deviations

were identified.

0 erational Staffin

- Unit 3

During this inspection,

the inspector

reviewed the qualifications

and level of experience

of managerial

and operations

support staff

personnel

responsible for the performance of maintenance,

instrument

calibration,

and surveillance testing in Unit 3 for conformance to

the licensee's

FSAR commitments to ANSI/ANS 3. 1-1978.

On a station

level, this included

a review of the qualifications

and experience

21

of the individuals currently holding the following staff positions:

Plant Maintenance

Manager,

Mechanical

Maintenance

Supervisor,

Electrical, Maintenance

Supervisor,

and

I8C Maintenance

Supervisor;

and

on a unit specific level, the qualifications

and experience

of

the unit Mechanical

Maintenance

Superintendent,

Electrical

Maintenance

Superintendent

and I8C Maintenance

Superintendent

and

four mechanics,

four electricians

and four I8C technicians

working

in Unit 3.

All were found to meet or exceed

the minimum specified

requirements.

No violations of NRC requirements

or deviations

were identified.

ualit

Assurance for Measurin

and Test

E ui ment

M&TE - Unit 3

During this inspection,

the inspector

reviewed the licensee's

program

and procedures

for the control

and calibration of measuring

and test equipment

(M&TE) used in the performance of safety-related

maintenance,

calibration and surveillance testing of permanent plant

equipment in Unit 3.

The program

and administrative controls

associated

with the

use of M&TE

are the

same for all three units at

Palo Verde and

as

such

have

been

reviewed during previous

inspections.

The following program

and administrative control

procedures

were again reviewed

as

a part of this inspection with

emphasis

placed

on the review of recent

changes:

34P R-OZZ01

34AC-OZZ03

34AC-OZZ04

34AC-OZZ05

34AC"9ZZ07

34AC-9ZZ08

Measuring

and Test Equipment

(M8TE) Control

Program

Control of Nonconforming Measuring

and Test

Equipment

(M8TE) and Calibration Standards

Control of Automated Measuring

and Test Equipment

(M&TE) Calibration Programs

Control of Shipping,

Packing

and Receiving Inspection

of M8TE and Calibration Standards

M&TE Users Administrative Requirements

M&TE Work Control

The inspector also reviewed

a selection of generic calibration

procedures

for specific pieces of M&TE.

The inspector

peyformed

an

inspection of the licensee's

M&TE calibration and storage

facilities.

The inspector,

in particular inspected

the areas

in

Unit 3 where

M&TE is stored

and discussed

with licensee

personnel

in

Unit 3 the manner

in which pieces of M&TE are checked out and usage

recorded.

A sample of different pieces of M&TE including electrical

multimeters,

pressure

gauges

and torque wrenches

were examined for

indication of current calibration.

During the course of this

inspection,

the inspector did note

a sizeable

backlog in the number

of out-of-tolerance

notices awaiting final evaluation

by the

licensee.

This was discussed

with the licensee.

The licensee

did

present

the inspector with some evidence that the backlog was

diminishing; however, the inspector indicated to the licensee that

continued effort in this area

appeared

warranted.

The inspector

will follow the licensee's

actions to reduce the backlog of out-of-

tolerance

notices

(530/87-12-01).

22

No violations of NRC requirements

or deviations

were identified.

19.

TMI Action Plan Items - Unit 3

a.

Closed) II.E.4.2 - Containment Isolation

De endabilit

NUREG 0737, Clarification of TMI Action Plan Requirements,

lists six different criteria that should

be met by licensee's

to ensure

containment isolation dependability.

There should

be diversit

in

arameters

sensed for

initiation of containment isolation.

Per the Unit 3 Proof and Review Technical Specifications,

two different parameters

are

sensed for contaiment

isolation.

Containment pressure

of 3.0 psig or pressurizer

pressure

of 1837 psia will initiate a containment isolation

actuation signal

(CIAS).

A CIAS can also

be initiated

manually.

2)

Determine which

s stems enterin

Containment

are essential

and which s stems

are nonessential

and modif their

containment isolation accordin

1

The licensee's

definitions of essential

and nonessential

were documented

in the Lessons

Learned

Implementation

Report (LLIR) and were found acceptable

by NRR,

as

documented

in the Palo Verde Safety Evaluation Report

(SER), with two exceptions.

Seal injection and charging

lines were considered

to be essential

systems

by the

licensee

and are not isolated

on a CIAS.

Valves. CH-HV-524

and CH-HV-255 can manually isolate these lines from

Containment but were originally not supplied with Class

IE

power.

NRR required that these

valves

be supplied with

Class

1E power.

The inspector verified that

a

modification has

been completed,

which supplies

Class

IE

power to these valves.

All other non-essential

systems

are automatically isolated

on

a CIAS. This was verified by

reviewing procedure

93PE-3SAOl, "Integrated Test of

Engineered

Safety Features".

3)

Resettin

the

CIAS should not result in the automatic

reo enin

of containment isolation valves.

The inspector verified by review of procedure

93PE-3SAOl

that containment isolation valves

do not reopen

when a

CIAS is reset.

4)

The containment

ressure

set oint that initiates

a CIAS

should

be reduced to the lowest

ractical.

23

For Palo Verde, the original setpoint

was

5 psig and was

subsequently

lowered to 3 psig.

5)

Containment

ur e valves that do not satisf

certain

o erabilit criteria must be sealed

closed

and verified to

be closed at least ever

31 da s.

The inspector verified that surveillance test procedure

43ST-3CP02

implements this for the containment

purge

valves.

6)

Containment

ur e valves should close

on a hi

h radiation

sicinal.

The inspector verified that area radiation monitbrs

RU-37

and

RU-38 initiate a containment

purge isolation actuation

signal

(CPIAS) at a setpoint of 2.5 mrem/hr.

The inspector

was satisfied that the licensee

had properly

implemented this TMI Action Plan Item and it is closed.

b.

Closed

II.F. 1.2D Post Accident Monitorin

Instrumentation

Containment

Pressure

Monitor .

The inspector verified that the licensee

has installed

two

dedicated

containment pressure

transmitters,

with a range of -5

to +180 psig, to monitor containment pressure after an

accident.

The transmitters

were supplied

by Rosemount

and

qualified both seismically

and environmentally per Rosemount

Procedure

1802,

Revision A.

This was documented

per

ANPP

program

number 13-JM-311.

The inspector also verified that procedure

92GS-OZZ80 performed

the generic calibration of these

Rosemount pressure

transmitters.

The licensee

has satisfactorily implemented this TMI item and

it is closed.

As part of the inspection of these

TMI items, the inspector

reviewed

the portions of the Palo Verde

SER dealing with these

two THE Action

Plan Items.

The inspector verified that commitments

made

by the

licensee

in the Palo Verde LLIR concerning these Action Plan Items,

which were referenced

by

NRR in the

SER in determining acceptability

of the licensee's

proposed actions,

had in fact been

implemented.

No violations or deviations

were identified.

20.

Com arison of As-Built Plant to

FSAR Descri tion - Unit 3

The following systems

were reviewed to verify that the as-built

plant conforms to the commitments

contained in the

FSAR:

0

24

High Pressure

Safety Injection

Low Pressure

Safety Injection

Containment

Spray

Iodine Removal

Shutdown Cooling

Safety Injection Tanks

Auxiliary Feedwater

Essential

Cooling Water

The inspector

reviewed portions of isometric drawings,

Technical

Specification

(TS) surveillances,

and performed detailed field

walkdowns using the Piping and Instrumentation

Diagrams

(PAID) and

FSAR descriptions for the listed systems.

The field walkdowns

included piping, valve,

and instrumentation installation

and

numbe'ring,

including Control

Room indications

and controls,

where

applicable.

In all cases

reviewed,

the isometric drawings reflected the as-built

status of the plant.

However, the inspector identified three

cases

where the

PKIDs did not reflect the as-built installation.

In each

instance

the

P8 ID was in error.

One

P8 ID had not been revi sed when

a plant change

was

made.

The others

had been

drawn incorrectly on

the original revisions.

The inspector considered

the drawing

discrepancies

to be of a minor nature.

The licensee

reviewed these

instances

and concluded that they had

no effect on the operability

of the systems.

However, the licensee

implemented

drawing changes

at each unit to bring the P8IDs in conformance with the as-built

plant design.

The inspector also verified by sampling, that

TS

surveillances

for the reviewed systems

could be performed in the

as-built plant.

No violations of NRC requirements

or deviations

were identified.

21.

Followu

of Generic Letters - Units 1

2

and

3

a.

Closed

Generic Letter 85-22: Potential for Loss of Post-LOCA

Recirculation

Ca

abc lit

Due to Insulation Debris Slocka

e

The inspector observed that the licensee

had pursued

the review

recommendations

discussed

in NRC Generic Letter 85-22.

A

~ report summarizing the licensee's

evaluations

was noted by the

inspector to address

emergency

core cooling system

(ECCS)

sump

design

based

on debris effects,

degree of screen

blockage,

hydraulic performance,

and venting as

recommended

by Generic Letter 85-22.

The report concluded that the existing

ECCS

sump design

meets

the requirements/guidance

of Regulatory Guide 1.82,

Revision

1

and Standard

Review Plan, Section 6.2.2,

Revision 4.

This item

is closed for Units 1, 2,

and 3.

b.

Closed

Generic Letter 85-06:

ualit

Assurance

Guidance

For

ATWS

E ui ment That Is Not Safet -Related.

25

On June 1, 1984,

the Commission -approved publication of a Final

Rule,

10CFR 50.62,

regarding the reduction of risk from

anticipated transients

without scram

(ATMS) events for

light-water cooled nuclear power plants.

Section 50.62(d) of

the rule required that each licensee

develop

and submit

a

proposed

schedule for meeting the requirements

of the rule.

This generic letter (GL) was issued to provide explicit quality

assurance

guidance for non-safety-related

equipment

encompassed

by the

ATMS rule.

The licensee

provided their initial response

on October 12,

1985,

(ANPP-33712)

and stated that they are

a participant in

the Combustion Engineering

Owners

Group

(GEOG) program for

compliance with the

ATMS Rule.

The licensee

adopted

an initial

schedule

based

on the

GEOG program completion.

However,

on

February

24,

1987, the

NRC extended

the deadline for

implementation of the

ATMS rule requirement to no later than

the thir d refueling outage after July 24,

1984.

The current

implementation

schedule

for Palo Verde Units 1, 2,

and

3 is

prior to the third refueling after July 24, 1984, for each

unit.

The inspector verified that the licensee's

review and response

to this

GL was adequate

and timely.

Therefore, this item is

closed for Units 1, 2, and 3.

22.

Followu

I.E. Bulletin 86-03: Potential

Failure of Multi le

ECCS

Pum

s

Due to Sin le Failure of Air-0 crated Valve in Minimum Flow

Recirculation Lines - Unit 1

2

and

3

.

This Bulletin discusses

findings at several

plants whereby the

minimum flow recirculation lines for'oth

ECCS trains were returned

to a common header

and utilized .common air operated

valves to

isolate the line.

It was determined that

a single valve failure in

this recirculation line could prevent

minimum pump flow during

conditions in which the reactor coolant system pressure

was higher

than the shut off head of the

ECCS pumps.

Mithout minimum flow, the

pumps could overheat,

become

damaged,

and not able to perform their

intended safety functions.

The bulletin directed the licensee

to

review their

ECCS system to determine if a failure in the minimum

recirculation flow line could effect both trains of ECCS.

The

inspector

performed

an independent

review of the

ECCS systems

using

plant piping and instrumentation

drawings

and by walking down the

respective

High Pressure

Injection (HPSI),

Low Pressure

Injection

(LPSI) and Containment

Spray

(CS) systems for both trains.

Each

pump has

a miniflow line with a normally open, motor-operated

valve.

Each valve is supplied with Class lE power and fails-as-is

(open)

upon

a loss of power.

The miniflow lines for each train combine

into a single header for each train with a solenoid operated

isolation valve in each line.

These valves are powered from the

Class

1E 125V

DC system

and are energized to open.

The headers

then

combine into a single line going to the Refueling Mater Tank (RMT).

There are

no valves in this line.

26

The licensee

concluded that there is no single failure that would

cause multiple trains of ECCS

pumps

or valves to become

inoperable

and

no actions

were required.

The inspector verified that the

licensee's

review and response

to this item was comprehensive

and

timely.

Therefore, this item is closed for Units 1, 2,

and 3.

23.

Licensee

Event

Re ort

LER

Followu

- Units 1 and

2

a e

The following LERs associated

with operating

events

were

reviewed by the inspector.

Based

on the information provided

in the report, it'as concluded that reporting requirements

had

been met, root causes

had

been identified,

and corrective

actions

were appropriate.

The below

LERs are considered

closed.

Unit 1

LER NUMBER

DESCRIPTION

LERs 86"55-00,

01

Late Surveillance

Due to Hydramotor

Actuator Failure

LER 86-62-00

Late Surveillance

Oue to Communication

Error

LER 87-01-00

LER 87"07-00

Disabled

ESF Function (Documented in

paragraph

7)

Unit 2

LER NUMBER

DESCRIPTION

ESF Actuation Caused

By a Voltage Spike

LER 86-38-00

LCO Entry Oue to Inoperable

MSIVs

LER 86-42-00

Surveillance Test Performed

Late

Oue to

Personnel

Error

LERs 86-46-00,

Inadvertent

SIAS Oue to Manual Actuation

Ol

Handswitch Malfunction

LER 87-01-00

Personnel

Error Caused

Control

Room Ventilation

Monitors to be Inoperable

No violations of NRC requirements

or deviations

were identified.

24.

Followu

of 10 CFR 50.55

e

Re orts

DERs

- Unit 3

'a 0

The inspector reviewed

a sample of OERs that the licensee

had

dispositioned

as

Not Reportable

under the criteria of 10 CFR 50.55(e).

This review was conducted in order to evaluate

the

thoroughness

of the licensee's

analysis

and the validity of the

conclusions.

The following DERs were reviewed:

I

~

~

27

86-01

86-05

Nozzle-to-Shell'Welds

on

ASME III Tanks

and Heat

Exchangers

Weld Discrepancy

on

CE Supplied Transmitter

Racks

86-08

86-20

Grinnell ¹2 Sway Strut Clamp Interference

HVAC Damper Seals

Do Not Meet Required

Specifications

86-30

Equipment gualification Problems with Various

Fuses,

Terminal Blocks,

and Wiring

Each

DER provided

a complete description of the discrepant

condition and the evaluation of safety significance.

Also, the

root cause

and corrective action for each condition were

appropriately identified.

These

DERs are therefore

closed.

In

addition,

based

on the thoroughness

and completeness

of the

reports the inspector

reviewed, all other

DERs that have

been

dispositioned

as Not Reportable

are closed

and are listed

below.

86"03

Failure of Fire Hazards Analysis to Identify

Spaces

Between Buildings as Separate

Fire Areas

86-09

86-10

86-11

86-16

86"22

86-23

86-25

PASS Deficiencies

Saturation of Radiation Monitoring Instruments

gualification of Skinner Solenoid Valves

Lack of Calculations for Conduit Supports

Redundant Fault Current Protection

Broken Nut on ¹1

SG Sliding Base Support Forging

Wrong Conversion Factors

on RU-1 Radiation

Monitor

86-26

86-32

86-41

Softer Than Required

Nuts with Heat Trace

6C

Discrepancies

Found Between

Pipe Support Designs

and Stress

Analysis Calculations

Required

DCPs

May Not Have Been Incorporated

on

Some Limitorque Operators

87"01

87-05

Brown-Boveri Circuit Breakers with Possible

Damaged Wires in Wire Harnesses

Potential

Problems with g-Class

HVAC Damper

Actuators

v

28

87-08

Possible

Problems with Limitorque Wire

Degradation

in g-Class

DC tlotors

b.

Finally, the inspector

reviewed

and closed the following

Reportable

DERs:

85-38 Deficiencies Identified Durin

Audit of General

Electric

GE

Com an

.

A safety concern

was identified by the licensee

wherein

GE

was processing

the purchase

of safety grade materials

as

commercial

grade.

The root cause

was attributed to a

change in a

GE computer program in June,

1985 that

triggered the processing

of Class

1E orders

as commercial

grade.

As part of their corrective action,

GE committed

to review all spare

and replacement

procurements

supplied

to Palo Verde.

All suspect

material

has either

had the

purchase

order cancelled,

been returned to GE,

has

been

subsequently certified, or been quarantined

unti 1

certification could be established.

In only two cases

were commercial

grade material actually installed in Class

lE applications.

Two terminal blocks were installed in

safety grade switchgear in Unit 3.

The licensee

has

committed to relacing these parts with qualified terminal

blocks per

WOs 184631

and 188339, prior to fuel load.

This

DER is closed.

2)

86-31 Loose Diesel Generator

Rotor Windin s

While doing normal maintenance

of the Unit 3 "B" Diesel

Generator,

the licensee

discovered that the copper

windings of one of the rotor poles were loose.

Centrifugal force had apparently

broken the resin

bond and

the wires separated

from each other.

The root cause

was

attributed to improper application of the resin

bond on

the wire-wound rotor pole.

The defective rotor pole piece

was replaced.

The licensee

also discovered

loose pole piece fasteners

during the examination of the defective rotors.

The

vendor supplied the proper torque values for the fasteners

and they were retorqued

by the licensee.

The licensee's

corrective action for these deficiencies is

considered

adequate

and this

DER is closed.

3)

86-47 Diesel Generator

En ine Failure

The Unit 3 "B" Diesel Generator failed catastrophically

during the performance of a fully loaded 24-hour run as

part of a preoperational

test.

29

The diesel

engine sustained

major damage to cylinders,

pistons,

connecting

rods, articulating rods

and other

components.

The root cause

was determined to have resulted

from a

layer of electroplated

iron on the surface of one piston

rod.

This electroplated

iron was

used to repair the

overmachining of the surface.

A crack was initiated in

the iron and it propagated

into the base metal.

The

piston rod thus failed and was ejected out the side of the

diesel

engine.

Corrective action for this event included replacement

of

any iron plated piston rods in all other diesel

generators

at the Palo Verde site.

In addition, all the remaining

rods in both diesels

in Unit 3 have

been ultrasonically

tested

and

no crack indications identified.

Repair of the "B" Diesel Generator is ongoing and will be

followed by the resident staff.

This

DER is closed.

No violations of NRC requirements

or deviations

were identified.

25.

Review of Periodic

and

S ecial

Re orts - Units 1 and

2

Periodic

and special

reports

submitted

by the licensee

pursuant to

Technical Specifications 6.9. 1 and 6.9.2 were reviewed

by the

inspector.

This review included the following considerations:

the report

contained

the information required to be reported

by

NRC require-

ments; test results

and/or supporting information were consistent

with design predictions

and performance specifications;

and the

validity of the reported information.

Within the scope of the

above,

the following reports

were reviewed by the inspector.

Unit 1

Monthly Operating Report for January,

1987.

1-SR-86-053

Reactor Trip in Units 1 and

2 due to Loss of Startup

Transformer

1-SR-86-068

Inoperable

Seismic Monitoring Instrumentation

1-SR-86-069

Inoperable

RVLMS

1-SR-'86-069-1

One Inoperable

Channel of RVLMS

1-SR"86-079

Reactor Trip and

ESFAS

Due to Spurious

Reactor

Coolant

Low Flow

1"SR-86-085

Notice of Unusual

Event Due to SIAS from Feedwater

Control

Problems

30

1-SR-86-087

RU-1 Removed

from Service for Calibration

1-SR-86-089

RU-146 Out of Service Greater

Than 72 Hours

1-SR-86-097

RU-145 Out of Service

1-SR-86-093

Containment

Area

Rad Monitor Inoperable for Greater

Than 72 Hours

1-SR-87-005

Radiation Monitoring Unit Inoperable

Oue to Closed

Valve

1-SR-87-009

Steam Generator

Tube Plugging

Unit 2

Monthly Operating

Report for January

and February,

1987.

2-SR-86-028

Radiation Monitor Inoperable for Greater

Than 72

Hours

2-SR-86-030

RU-1 Inoperable for Greater

Than

72 Hours

2-SR-86-031

RU-142 Failure

2-SR-86-032

Containment

Rad Monitor

Inoperable Greater

Than

72 Hours

2-SR-86-033

RU-146 Failure

2-SR-86-036

RU-1 Inoperable Greater

Than

72 Hours

2-SR-86-037

RU-1 Inoperable Greater

Than 72 Hours

2-SR-86-039

RU"1 Inoperable Greater

Than 72 Hours

2-SR-87-001

RU-144 Inoperable for Greater

Than 72 Hours

No violations of NRC requirements

or deviations

were identified.

26.

Unresolved

Items

Unresolved

items are matters

about which more information is re-

quired to determine whether they are acceptable,

violations or

deviations.

Unresolved

items addressed

in this inspection are

contained in paragraphs

7 and ll of this report.

The inspector

met with licensee

management

representatives

period-

ically during the inspection

and held an exit on April 3, 1987.

31

The scope of the inspection

and the inspector's

findings,

as noted

in this report,

were discussed

and acknowledged

by the licensee

representatives.

L