ML17292B251

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Insp Rept 50-397/97-20 on 971221-980131.Violations Noted. Major Areas Inspected:Maint,Engineering & Plant Support
ML17292B251
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 02/19/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML17292B249 List:
References
50-397-97-20, NUDOCS 9802250114
Download: ML17292B251 (30)


See also: IR 05000397/1997020

Text

ENCLOSURE 2

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket No.:

50-397

License No.:

NPF-21

Report No.:

50-397/97-20

Licensee:

Facility:

Location:

Washington Public Power Supply System

Washington Nuclear Project-2

Richland, Washington

Dates:

December 21, 1997, through January 31, 1998

Inspectors

S. A. Boynton, Senior Resident Inspector

T. R. Meadows, Reactor Engineer

G. W. Johnston, Senior Project Engineer

M. P. Shannon, Senior Radiation Protection Specialist

Approved By: H. J. Wong, Chief, Reactor Projects Branch E

ATTACHMENT: Supplemental Information

9802250ii4 9802i9

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ADQCK 050003'P7

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EXECUTIVE SUMMARY

Washington Nuclear Project-2

NRC Inspection Report 50-397/97-20

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The professionalism of the control room operators and shift management ownership of

crew activities supported good operational performance over the inspection period.

Operators were generally knowledgeable of plant and equipment status, with several

minor exceptions (Section 01.1).

The licensee's program to assure that corrective lenses for self-contained breathing

apparatus (SCBA) for operators requiring them was implemented successfully. However,

procedural guidance for maintenance of the SCBA corrective lens program was

considered weak in that periodic inventories were not required and written expectations

were not provided to operators on the need to have SCBA qualified lenses, regardless of

the type of corrective lenses normally used (Section 01.2).

A personnel error on the part of an equipment operator during the performance of

clearance order activities resulted in the momentary deenergization'of the Division II

4160V vital bus and the loss of residual heat removal assist cooling of the spent fuel

pool. A noncited violation was identified associated

with this 1996 licensee event report

(Section 08.1).

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Observed maintenance and surveillance activities were generally well coordinated and

executed with appropriate craft supervision and system engineering participation

(Section M1.1).

The failure of maintenance

personnel to read and adhere to the instructions on a caution

tag prior to manipulating a breaker resulted in the loss of the Division I 125VDC critical

instrument power inverter, the initiation of several essential safety features, and isolation

of several containment isolation valves.

The event occurred while the plant was defueled

in Mode 5. A noncited violation was identified associated with this 1996 licensee event

report (Section M8.1).

~En ineeiin

Licensee procedures for controlling the configuration of the 4160V vital switchgear

breakers did not ensure that configurations would be consistent with the seismic

qualification of the switchgear.

A noncited violation was identified associated with this

1996 licensee event report (Section E8.1).

Calibration and surveillance procedures for the rod block monitor system were found to.

be inadequate to ensure the rod block monitors were operable prior to exceeding

30 percent rated thermal power as required by Technical Specifications.

As a result, the

-3-

system did not enforce rod blocks until power was approximately 33 percent.

A noncited

violation was identified for this 1997 licensee event report (Section E8.2).

In establishing the flow switch high flow isolation setpoint for the reactor water'cleanup

system blowdown line, engineering personnel did not adequately review the instrument

loop design.

This resulted in the application of an improper conversion factor for the flow

switch and a nonconservative high flow isolation setpoint that exceeded the maximum

allowable Technical Specification value. A noncited violation was identified associated

with this 1997 licensee event report (Section E8.3).

~

Three examples were identified in which the licensee had evaluated and implemented a

change to the facility, as described in the Fina1'Safety Analysis Report, but failed to

update the report in accordance with 10 CFR 50.71(e).

The licensee is implementing a

broad review of the Final Safety Analysis Report to identify and correct any additional

errors. A noncited violation was identified (Section E8 4).

~

Corrective actions to address inadequate labeling of radioactive material containers have

not been effective in'preventing recurrence, as evidenced by several recent

noncompliances identified by the inspectors and the licensee, and resulted in a violation

of 10 CFR 20.1904(a).

Additionally, a lack of defined ownership of areas in the radwaste

building contributed to poor radiological housekeeping

practices on the 507 foot elevation

(Section R1.1).

Engineering controls placed upon the traversing in-core probe Drive C were

insufficient'n

preventing movement of the probe during troubleshooting activities. The unexpected

movement of the probe required personnel actioh to.prevent the probe from withdrawing

from its shielded location and going into the area where the troubleshooting was being

performed.

Based upon other barriers to personnel overexposure that were in place and

the immediate actions taken in response to the event, the likelihood of a significant

overexposure was low (Section R1.2).

The licensee's analysis and root cause evaluation of the unexpected movement of the

traversing in-core probe accurately characterized the event and identified a number of

areas for improvement, including personnel level of knowledge of TIP system operation

and level of involvement of radiation protection supervision in the ALARAplanning

process for high radiological risk jobs (Section R1.2).

Summa

. f Plan

S a

The plant began the inspection period at 100 percent power. On January 12, power was

reduced to approximately 99 percent when the licensee identified a minor but nonconservative

input error to the plant process computer's heat balance calculation.

The licensee corrected the

error and returned the plant to full power on January 22. The plant remained at 100 percent

power for the balance of the inspection period.

01

Conduct of Operations

01.1

en

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s

707

During the inspection period, the inspectors performed extended observations of the

conduct of activities in the control room. Allsix crews were observed during

approximately 75 hours8.680556e-4 days <br />0.0208 hours <br />1.240079e-4 weeks <br />2.85375e-5 months <br /> (including 26 shift turnoyers) of observation in the control room.

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The operators were generally alert, responsive to alarms, professional, and safety

conscious.

The inspectors observed that operators used good operator self-checking

when manipulating controls and three-way communication when appropriate.

The

inspectors observed appropriate shift management involvement in daily activities. Shift

turnovers were thorough, efficient, and covered all plant activities planned for the shift.

The shift supervisor also reviewed any problem evaluation requests (PERs) and new

night orders.

When questioned on various aspects of plant'status and systems,

operators were generally found to be knowledgeable, except as noted below:

During a morning shift crew briefing, the inspectors noted that the night shift crew

had turned over to the oncoming crew that the off-gas condenser level controller

had to be vented due to a buildup of gas.

When questioned, the oncoming crew

did not know the reason for the gas buildup and had accepted the venting as

routine. Subsequent

investigation by the licensee identified a faulty level

controller and the problem was corrected.

A review of control board process parameters

noted that the indicated flowfor

Main Steam Line A was approximately 8 to 9 percent lower than the other three

steam lines.

From questioning operators from several different crews, the

inspectors determined that none of the operators could adequately explain the

difference in the flow indications.

In subsequent

discussions with the cognizant

-2-

system engineers, the inspectors found that the flow difference is a physical

phenomenon that resulted from the licensee's main turbine governor valve

optimization modification.

Operating Instruction (Ol) 9, "Expectations for Supervisory and Peer Oversight," provides

guidelines for reinforcing performance expectations and coaching of the operations staff

through direct observation of routine activities. Ol-9 also delineates the number of

observations that each of the members of the shift crews are expected to perform on a

shift or weekly basis.

A review of the observations performed by each of the six crews

during the months of December and January found that the expectations of Ol-9 were

generally being met. The number of observations performed within each crew also

showed a renewed emphasis on implementing the Ol-9 program at the crew level. The

inspectors concluded that this level of coaching likely contributed to the good

performance during December and January.

It was also recognized that performance

was improved from similar periods during the past several years.

Qgni~us'i~

The professionalism of the control room operators and shift management ownership of

crew activities supported good operational performance over the inspection period.

Operators were generally knowledgeable of plant and equipment status with several

minor exceptions.

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The inspectors verified operator license conditions regarding operator licenses which

specified the need for corrective lenses.

The inspection included a review of the

licensee's processes

for ensuring that SCBA qualified corrective lenses were readily

available in the control room.

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Licensed operators who, as a condition of their license, are required to wear corrective

lenses during the performance of licensed activities, 'are also required to have SCBA

'qualified corrective lenses readily available in the control room. The inspectors

interviewed two operators with conditions for corrective lenses and were informed that

SCBA qualified lenses were in individual lockers in the control room. The inspectors also

verified that the licensee has administrative and training procedures

in place that require

biennial SCBA fit tests and reminders for operators to check that they have SCBA

qualified lenses, ifnecessary.

However, the inspectors found that the licensee did not have in place instructions or

procedures that require an independent periodic inventory of SCBA qualified lenses for

-3-

licensed operators in the control room. The licensee also did not have a system that

could readily list which operators are required to have SCBA qualified lenses.

The

inspectors found from interviews with licensee management that it was their expectation

that all licensed operators that have licenses with conditions for corrective lenses have

SCBA qualified lenses readily available, whether or not they normally wear contacts or

glasses.

However, this expectation was not communicated to operators in writing.

Operations management committed to revise their conduct of operations procedures to

require licensed operators to periodically verify inventory for their SCBA qualified

corrective lenses, as necessary.

The licensee also committed to provide written

expectations of their policy regarding SCBA qualified corrective lenses.

The lack of

procedural guidelines and written expectations to require and monitor the continued

availability of SCBA qualified corrective lenses in the control room was considered a

weakness

in the implementation of the SCBA program.

c.

~Cncl sion

The licensee's program to assure that corrective lenses for SCBA for operators requiring

them was implemented successfully.

However, procedural guidance for maintenance of

the SCBA corrective lens program was considered weak in that periodic inventories were

not required and written expectations were not provided to operators on the need to have

SCBA qualiTied lenses, regardless of the type of corrective lenses normally used.

Operational Status of Facilities and Equipment

02.1

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71707

The inspectors walked down accessible portions of the following engineered safety

feature systems:

Control Room Ventilation

Emergency Diesel Generators

(Div. I, II, III)

4160V Vital Switchg ear

Standby Service Water System (Train A)

Each of the systems was found to be properly aligned for the current plant conditions.

Material condition of system components was found to be generally good, with

deficiencies properly identified. However, during tours of the emergency diesel

generator (EDG) rooms, the inspector found the "Ready for AUTO Start" light on the

Division II EDG local control panel and the "ON" light for Division III Fan DEA-FN-31 not

lit.

Subsequent

investigation by the licensee showed that the indicating lights had

burned out. Failed indicating lights on the diesel generator motor control centers were

noted as a concern in NRC Inspection Report 50-397/97-14.

4

08

Miscellaneous Operations Issues (92901)

08.1

Closed

LE

0-397/96002-00:

inadvertent loss of power to vital bus and automatic

start of associated

EDG. On May 4, 1996, with the reactor defueled, critical safety

Bus SM-8 lost power when supply Breaker 3-8 tripped open due to personnel error. As a

result, the Division II EDG started, the backup transformer automatically provided power

to Bus SM-8, and residual heat removal Pump 2B lost power. This pump had been

supplying fuel pool cooling in the assist mode.

The plant was immediately restored to

normal lineup. The licensee determined the cause of the event was momentarily

opening of the Bus SM-3 potential transformer (PT) fuse compartment by an equipment

operator (EO). The EO had erroneously opened and then reclosed the PT compartment,

leaving it in an abnormal condition. The EO was installing clearance orders in and

around Bus SM-8.

The licensee took the following immediate actions:

~

Operations management suspended

ongoing clearance order restoration

activities and initiated a PER

.

~

Residual Heat Removal Pump 2B was returned to service within 45 minutes.

I

The licensee took the following additional corrective actions:-

Revised procedures/instructions

regarding clearance order preparation to ensure

the need for simultaneous verification is noted.

Took appropriate personnel action against the EO.

Counseled the production reactor operator and senior reactor operator that were

involved concerning the necessity of performing adequate

prejob briefs prior to

performance of critical clearance activities.

Because the licensee event report (LER) did not address labeling of the fuse

compartments as a potential contributor, the inspectors independently observed the

associated

Bus SM-3 fuse panels and found them to be well labeled.

The inappropriate

opening of the Bus SM-3 PT fuse compartment was determined to be a violation of the

licensee's clearance order procedure and Technical Specification (TS) 6.8.1.a.

This

nonrepetitive, licensee-identified and corrected violation is being treated as a noncited

violation consistent with Section VII.B.1 of the NRC Enforcement Policy (NCV 50-

397/97020-01).

08.2

Closed

VIO 50-397/96003-02:

failure to draw a reactor coolant chemistry sample within

2-6 hours following a power change of greater than 15 percent, in accordance with

TS 3.4.5. The licensee determined that the root cause of the violation was an

inadequate procedure.

Specifically, the licensee found that neither Plant Procedure

0

-5-

Manual (PPM) 3.2.1, "Shutdown to Cold Shutdown," nor PPM 3.2.2, "Shutdown to Hot

Shutdown," contained steps in the body of the procedure to notify chemistry of the need

to perform a sample following the recirculation pump shift, an evolution that resulted in a

.power change of greater than 15 percent.

A prejob brief that failed to identify a

responsible individual to track reactor power changes and notify the chemistry

department and insufficient information in the control room log identifying specific power

changes were considered to be contributing factors.

In addressing the root cause and contributing factors, the licensee revised PPMs 3.2.1

and 3.2.2 to include the assignment of an individual to track reactor power changes and

to notify chemistry, as appropriate.

A performance improvement plan was implemented

to address critical behaviors for effective crew prejob briefs while the licensee's

performance oversight process was also revised to include a prejob brief observation as

a performance feedback tool.

The inspectors noted that the licensee's Improved Technical Specifications, implemented

in March 1997, no longer require a reactor coolant system sample to be drawn when

reactor power is changed by greater than 15 percent in a 1-hour period.

M1

Conduct of Nlaintenance

M" .

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e

2707

The inspectors observed and/or reviewed the following maintenance and surveillance

activities:

Work Order Task HJJ301, Off-gas Hydrogen Analyzer B Channel Check

Work Order Task JRJ701, Service Water Process

Radiation Monitor Adjustment

Work Order Task HVB001, Reactor Building Fan ROA-FN-1B Lubricate Bearings

Work Order Task HTZ901, Reactor Core Injection Cooling Water Leg Pump,

RCIC-P-3 Oil Change and Lubrication

Work Request 98000012, Reactor Water Feed GE FANUC CPU Scanner Module

Failure

Work Order Task JSZ6T2, Replace Reactor Heat Removal Pump, RHR-P-3,

Packing

-6-

Work Order Task HYR300, Replacement of Instrument Test Valves on Main

Steam Instrument Rack E-IR-H22/PO15

Work Request 98000009, WCH-DPT-50 AirSeparator Controller Reset

Work Order Task HML704, Standby Liquid Control Pump, SLC-P-2B,

Replacement of Lube Oil

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The inspectors observed that, with the one exception noted below, the work was

'performed professionally and was consistent with the licensee's work control procedures

and expectations.

The inspectors also observed frequent maintenance management

and operations personnel supervision and observation during this inspection period.

On January 15, 1998, the inspectors periodically observed craft personnel replace

lubricating oil on standby liquid control (SLC) Pump SLC-P-2B. On one occasion the

inspectors arrived at the work location and noticed tools and other loose items lying

about, with no licensee personnel and no work-in-progress sign present.

The inspectors

found that it is the licensee management

expectation to have an appropriately filled out

work-in-progress sign in place when it is necessary to abandon the work site. The

inspectors also observed that the personal protection shield over the motor-to-pump

coupling had been removed and the coupling left exposed.

The inspectors determined

that this was in accordance with the licensee's foreign material exclusion procedures

in

that the procedures only required foreign material exclusion for internal pump or motor

components.

However, the inspectors concluded that the missing sign, disarrayed tools,

and uncovered shaft coupling with the absence of personnel present to be poor work

practices which did not meet the licensee management expectations.

c.

Conctusiorcs

The observed maintenance

and surveillance activities were generally well coordinated

and executed with appropriate craft supervision and system engineering participation.

MS

Miscellaneous Maintenance Issues (92902)

M8.1

Closed

LE

50-397/96001-00:

inadvertent engineered safety feature (ESF) actuation

due to tripping temporary power supply. On April 25, 1996, two temporary electricians

inadvertently opened the fused disconnect supplying the uninterruptible power supply

Inverter IN-3 loads.

This caused

a loss of power to the loads and subsequent

ESF

actuations and containment isolations.

Since the plant was in an outage and defueled,

there was little impact and the operators quickly restored the affected systems.

Inverter IN-3 loads were being temporarily supplied through a disconnect switch that was

labeled as a spare breaker.

A caution tag on the disconnect handle identified it as the

-7-

temporary power supply to Inverter IN-3 with instructions to contact the control room

before operating the disconnect.

The two electricians said that they did not read the

caution tag. The licensee determined the'root cause of the event to be human error.

The licensee took the following immediate'actions:

~

Operations restored power to Inverter IN-3 loads and reset the ESF actuations

without further incident.

~

Restricted the two electricians from the power block for the remainder of the

outage.

~

Reiterated management expectations concerning equipment clearance

'requirements and the appropriate approvals needed prior to entering panels,

components,

or systems, during briefings with plant and contractor maintenance

personnel.

The licensee took the following additional corrective actions:

~

Revised PPM 10.25.1, "Maintenance Programs and Procedures," Revision 9, to

include the requirement to provide field identification of spare disconnects that

are providing temporary power.

~

Revised applicable maintenance lesson plans to include lessons learned from

this event regarding clearance orders and the opening of panels.

The failure of the electricians to read and adhere to the instructions on the supply

breaker's caution tag was identified as a violation of the licensee's clearance order

procedure and TS 6.8.1.a.

This nonrepetitive, licensee-identified and corrected violation

is being treated as noncited violation consistent with Section VII.B.1 of the NRC

Enforcement Policy (NCV 50-397/97020-02).

M8.2

Closed

Viola ion 50-397/

2-01: Plant Procedure Manual Procedure 2.10.4, "Diesel

Generator (DG) and Cable Cooling Heating Ventilation, and'Air Conditioning (HVAC),"

Revision 12, date January 11, 1996, did not provide adequate instruction for

troubleshooting for low DG room temperature conditions.

The procedure did not include

provisions for other possible causes,

such as the standby DG heating and ventilation unit

damper positions.

The licensee identified that, in past revisions, inclusion of checks of possible inleakage

past the emergency ventilation unit dampers was considered unnecessary.

This was

because the dampers were not thought to be likely sources of outside air inleakage.

The

licensee has included steps to check the dampers and to consider other possible

sources as contributors to cold room temperature

in Revision 13 to PPM

Procedure 2.10.4.

-8-

NRC Inspection Report 50-397/96-06 identified further examples of this violation.

Corrective actions for those specific violations included changes to PPM

Procedure 1.3.78 to further define management expectation of the use of emergency

maintenance.

PPM Procedure 1.3.78 was superseded

by Site Wide Procedure SWP-MAI-01, "Work

Management - Planning, Scheduling and Work Activities," Revision 0. The inspector

examined Procedure SWP-MAI-01 and determined that the procedure in Section 3.1

provides guidance that defines the circumstances under which emergency maintenance

can proceed.

The inspector concluded that the guidance was sufficient to ensure proper

control of emergency maintenance activities.

Procedure SWP-MAI-01 also provides guidance on management

expectations for

postmaintenance

testing and determination of operability. The inspector concluded that

guidance was sufficient to assure that adequate postmaintenance

testing is identified

and that testing is sufficient to determine operability.

The licensee's corrective actions were considered appropriate.

ES

INiscellaneous Engineering Issues (92903)

E8.1

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electrical breakers not seismically qualified in

test/disconnect

position.

On November 22, 1996, the licensee identified that the plant

was in an unanalyzed condition due to a spare electrical circuit breaker in a safety-

related 4160 V switchgear being in a racked out condition not assessed

by seismic

analysis.

Specifically, seismic testing of the vital 4160V switchgear was not conducted

with breakers in a racked out condition. The licensee immediately reported this condition

to the NRC and removed the spare breaker from the switchgear and placed it in a

qualified position.

The licensee concluded that the root cause of the event was the failure of the

manufacturer to test the vital switchgear with breakers in the racked out condition.

However, the LER further states that the switchgear was tested in accordance with

Electrical Standard IEEE-344, 1971, which only specifies testing in the service mounted

or racked in condition. The inspector considered the licensee's identified root cause of

the event to be inappropriate based on the IEEE testing requirements and the corrective

actions taken to address the issue.

The licensee's corrective actions included revising

procedures for racking out breakers to ensure that they are not placed in a nonseismic

qualified position. Also, seismic qualification files for existing safety-related switchgear

were revised to specify the lack of seismic qualification for breakers in the racked out

condition. The corrective actions taken were considered appropriate.

-9-

The failure of plant procedures and instructions to control the configuration of the vital

4160V switchgear to ensure that its seismic qualification was maintained was identified

as a violation of 10 CFR Part 50, Appendix B, Criterion III (Design Control). This

nonrepetitive, licensee-identified and corrected violation is being treated as a noncited

violation consistent with Section VII.B.1 of the NRC Enforcement Policy

(NCV 50-397/97020-03).

E8.2

Clo

d

ER

0- 97/97002-00:

rod block monitor calibration values not in accordance

with Technical Specifications.

On February 18, 1997, the licensee determined that they

were not in compliance with TS Table 3.3.6-1 and TS 3.1.4.3 regarding the operability of

the rod block monitoring (RBM) system.

A vendor surveillance procedure to calibrate

RBM channels caused an error that did not allow RBM to become operable until

33 percent power. The TS limitwas 30 percent power. This condition had existed since

the original plant startup.

The licensee also found similar errors in the TS RBM

surveillance procedures.

The licensee immediately corrected the vendor procedures,

recalibrated the RBM

channels, and reperformed the channel surveillance to verify that the RBM systems

became operable at 30 percent power. The licensee then revised the TS RBM

surveillance procedures to correct the errors.

The licensee also implemented the

Improved Technical Specifications which also checked or corrected other TS related

instrument surveilances.

The failure of the RBMs to be operable prior to exceeding

thermal power levels of 30 percent was considered to be a violation of TS 3.0.4.

The inspectors reviewed the corrective actions and found them to be acceptable.

However, the inspectors noted that the licensee's root cause analysis had not addressed

why operators did not identify the concern with the RBMs during the many plant startups

since the initial startup.

Current procedures do include a step to verify that the RBM

downscale alarm is clear prior to going above 30 percent power. This nonrepetitive,

licensee-identiTied and corrected violation is being treated as a noncited violation

consistent with Section Vll.B.1 of the NRC Enforcement Policy (NCV 50-397/97020-04).

E8.3

Clo ed

LER 50-397/97001-00:

reactor water cleanup (RWCU) blowdown flow isolation

setpoint above TS allowable limit. On February 11, 1997, the licensee determined that

they did not comply With TS 3.3.2 for the maximum allowable RWCU blowdown flow of

equal to or less than 271.1 gpm. The licensee determined that an improper dc voltage

setpoint for the associated

leak detection system flow switches had been used in the

original RWCU high blowdown flow isolation trip signal calculation.

The calculation error

was in the nonconservative direction. The licensee took the following corrective actions:

Immediately isolated RWCU blowdown flow.

Modified applicable channel calibration, channel functional checks, and response

time testing procedures to incorporate the corrected setpoints from the corrected

calibration.

0

-10-

Recalibrated applicable flow switches, realigned the RWCU system, and restored

blowdown capability.

Initiated a plan to conduct a review of plant instrument setpoint calculations and

associated

master data sheets.

The failure to set the flow switches to isolate RWCU prior to exceeding a blowdown flow

of 271.1 gpm was determined to be a violation of TS 3.3.2.

The inspectors reviewed the corrective actions and found them to be acceptable.

This nonrepetitive, licensee-identified and corrected violation is being treated as a

noncited violation consistent with Section VII.B.1 of the NRC Enforcement Policy

(NCV 50-397/97020-05).

E8.4

Clo

d

In

ec ion Followu

Item 50-397/9

0

- 4: failure to update the Final Safety

Analysis Report (FSAR). The inspectors identified three examples in which the licensee

made changes to the facility, as described in the FSAR, but failed to update the FSAR to

reflect those changes.

The three examples included:

Removal of the diesel-driven air compressor for the Division II EDG starting air

system (FSAR Section 9.5.6.2).

Removal from service of the 522 foot reactor building elevation electronics air

conditioning unit (FSAR Section 9.4.2.2.4.d).

Elimination of the electrohydraulic operator for Valve WOA-V-52D, control room

HVAC purge isolation valve (FSAR Section 6.4.4.1).

For each of these changes, the licensee had performed a written safety evaluation in

accordance with 10 CFR 50.59. As a corrective action to these and other examples

identified by the NRC and the licensee, the licensee has undertaken a broad program

review to identify any additional discrepancies

and update the FSAR. A description of

the licensee's program was provided in NRC Inspection Report 50-397/97-14.

From a

review of the scope and depth of the licensee's review program, the inspector concluded

that the licensee would likely have identified and corrected the above discrepancies.

The

, failure to update the FSAR was determined to be a violation of10 CFR50.71(e).

This

noncompliance is'eing treated as a noncited violation, consistent with Section VII.B.3of

the NRC Enforcement Policy (NCV 50-397/97020-06).

An inspection followup item will

be opened to evaluate the licensee's corrective actions for FSAR discrepancies

(Inspection Followup Item (IFI) 50-397/97020-07).

E8.5

Closed

Unresolved

I em

0-397/96026-04:

failure of standby service water Pump 1A.

Standby service water Pump 1A tripped unexpectedly on December 20, 1996, when

control room operators attempted to start the pump. This issue was closed in NRC

Inspection Report 50-397/97-04 in the review of LER 96009-00.

-11-

E8.6

I

d Ins

i n F Ilowu

I em

0-397/97018-0:

review of transient hydraulic loads

on standby service water loop piping. The licensee's analysis of service water Loop B

piping was documented

in Calculation Modific'ation Record ME-02-96-25. The

calculation was to evaluate the service water Loop B piping hydraulic transients in

response to PER 295-1 275. This IFI was initiated on closure of IFI 50-397/95033-01.

The results of the calculation'did not indicate there were any substantive stresses

imparted to the piping or supports.

At the time of NRC Inspection Report 50-397/97-18,

the inspector had not completed a review of the calculational methodology.

After the inspections, the licensee conducted an analysis of the effects of the water

hammer to quantify the stresses

incurred during the event.

The inspector reviewed the

calculation and determined that the methodology appeared

to be appropriate.

The

results of the calculation indicate low stress levels and no apparent potential for damage

to the piping. Maximum indicated stress to the piping itself was 842 psi, with an

allowable stress of 15,000 psi. For the pipe support lugs on the return line hanger at

SW-1063-12, where the highest stress was identified, the stress was 7,600 psi with an

allowable stress of 18,000 psi.

The inspector concluded that the calculations were appropriate, addressing the most

significant portions of the piping and confirming the observations of no damage to the

piping or supports.

IV. Plant Support

R1

Radiological Protection and Chemistry Controls

R1.1

In d

ua e

arkin

f Radioac ive M

erial

ntai

and R

i

i n

i n

a.

Inse in

e 7750

The inspectors conducted frequent plant tours to evaluate,

in part, radiation protection

controls and practices.

b.

bs rva ion

andFin

'n s

adi

iv

Ma erial Labelin

On December 31, 1997, while conducting a general tour of the 507 foot level of the

radwaste building, the inspectors found three sealed bags containing HEPA filters just

outside of a radiological work isolation room. The sealed bags were not labeled as to

any potential radiological hazard.

The inspectors also found a large internally

contaminated piece of machinery that was wrapped and sealed in a radiological control

bag which was also not labeled.

In addition, the inspectors noted an apparent

contamination control area that was posted with unmarked radiation signs.

On

-12-

January 22, 1998, the inspectors noted another radiological control bag that was

, apparently not labeled.

This was also found on the 507 foot level of the radwaste

building. Subsequent

investigation by the licensee found that'a label was attached to the

material inside the bag which was not readily visible to the inspector.

From discussions

with the radiation protection manager, this labeling practice did not meet management

expectations.

The unmarked radiation signs for the apparent contamination control area were a

concern because they lacked information on the general hazards within the area and

also have the potential to desensitize licensee personnel to radiation signs.

For each of

the sealed bags of contaminated equipment noted above, a clearly visible label could not

be identified that provided information on the quantity of radioactivity, radiation levels,

and kinds of material present.

The inadequate labeling of the radioactive material was

determined to be a violation of 10 CFR 20.1904(a) which requires containers of licensed

material be labeled with sufficient information to permit personnel to take precautions to

avoid or minimize exposures (VIO 50-397/97020-08).

The failure to properly label containers of radioactive material has been the subject of

several recent PERs.

PER 296-0346 was initiated due to an adverse trend in

compliance with the licensee's radioactive material labeling procedure.

Subsequent to

the initiation of PER 296-0346, 15 additional noncompliances with the labeling procedure

were identified, 3 of which occurred after closure of the PER. As a result, the licensee

initiated another adverse trend PER for those concerns (PER 296-0839).

The licensee's

root cause analysis showed that the earlier events were generally caused by errors

made by health physics technicians.

As a result, enhancements

were made to the

licensee's labeling procedure and specific training was provided to the health physics

technicians.

The licensee's review of the more recent concerns with labeling found that the errors

were generally caused by inadequate radiation worker performance.

Additional

improvements to plant procedures were implemented as a result. To improve radiation

worker performance,

it was also recommended,

through the disposition of PER 296-

0839, that a request be submitted to the cognizant training advisory groups (TAGs) to

address radioactive material labeling requirements. in their training programs.

However,

the request that was actually sent to the TAGs did not require any modifications to their

programs and only asked that the TAGs consider addressing this issue.

The inspectors

considered this to be an important corrective action that had weak implementation, due

to the open-ended

nature of the request to the TAGs.

PERs 297-0485, dated May 26, 1997, and 297-0721, dated August 15, 1997, were also

initiated due to inadequate labeling of radioactive material.

PERs 297-0485, 297-0721,

and the more recent examples identified by the inspectors indicate that the corrective

actions to improve radiation worker performance have not been fullyeffective.

0

-13-

Housekee

in

in Radiolo icall

C nrolle

Are s

On December 31, 1997, the inspectors noted anticontamination clothing loosely lying

about on the floor, just outside the step-off pad of a contaminated area of the 507 foot

. elevation of the radwaste building. On January 22, 1998, the inspectors again noted

poor housekeeping

practices on the 507 foot level of the radwaste building. Loose tools,

bolts, rope, and plastic straps were lying about both in and outside of controlled

contaminated areas near the step-off pad receptacles.

From discussions with the plant

manager,

it was determined that organizational ownership of the area was not clearly

defined for purposes of housekeeping

and cleanliness.

The radiation protection

manager walked down the areas noted by the inspectors and agreed that the

housekeeping

conditions found did not meet management

expectations.

Conclusions

Corrective actions to address inadequate labeling of radioactive material containers have

not been effective in preventing recurrence as evidenced by several recent

noncompliances identified by the inspectors and the licensee and resulted in a violation

of 10 CFR 20.1904(a).

Additionally, a lack of defined ownership of areas in the radwaste

building contributed to poor radiological housekeeping

practices on the 507 foot

elevation.

R1.2

E

ma

E

o ure Con

s

In

ec ion Sco e

8 75

On January 7, 1998, while troubleshooting was being performed on tiaversing in-core

probe (TIP) Machine C, withdrawal of the probe towards the TIP machine occurred

unexpectedly.

Selected radiation workers and radiation protection personnel involved in

the troubleshooting were interviewed. Additionally, the problem evaluation request which

documented the event was reviewed.

0 serva ions and Findin s

The inspectors reviewed Problem Evaluation Request (PER) 298-0019, which

documented the events associated

with the unexpected movement on January 7, 1998,

and found the PER and its associated

root cause evaluation to be an accurate reflection

of the event.

The inspectors determined that the root cause evaluation, including the

addendum, identified and captured a number of areas for improvement to help prevent a

similar occurrence

in the future.

During the review of this event, the inspectors interviewed the radiation protection

supervisor who had approved the radiation work permit (9700390-01) for the TIP drive

work and the radiation protection technician who performed the ALARAplan and

provided job coverage for the task.

Both of these individuals were under the mistaken

-14-

impression that the TIP could not fullywithdraw into the TIP drive room where the

troubleshooting was being performed on TIP Machine C.

From discussions with the

system engineer, he was aware that the TIP could fullywithdraw into the TIP drive room;

however, he was under the mistaken impression that the logic circuit was working

properly and would prevent this from happening.

As a result, the implemented

engineering controls were not comprehensive to ensure movement of the TIP probe was

precluded.

The inspector also concluded it was for this reason that the system engineer did not

discuss the possibility of the TIP completely withdrawing into the TIP drive room during

the ALARAprejob briefing with the personnel involved with this task.

From interviews with the radiation protection technician who performed the ALARA

planning aspects of the task, the inspectors determined that the radiation protection

technician researched

the plant's radiological job history files to identify past radiation

work permits and historical radiological survey information which was used for similar

work. However, the inspector found that the files did not contain industry events or NRC

information notices for similar work. The inspectors commented that maintaining industry

events and NRC information notices in job history files could help identify problems that

might be encountered.

The licensee acknowledged the inspectors'omment.

The licensee provided the inspectors an estimate of the worst case radiological

conditions in the event that the TIP was to completely withdraw into an unshielded

portion of the TIP system.

The licensee estimated, and the inspectors concurred, that

the radiation exposure levels could have been as high as 110 rems per hour at

30 centimeters (about

1 foot) from the TIP. The licensee's investigation determined that,

although the radiation protection personnel involved in the task knew that the exposure

rates could be substantial, they did not have a complete understanding of the radiological

conditions in the event the TIPs were fullywithdrawn.

The inspectors noted that the radiation protection supervisor who had approved the

radiation work permit was not involved in any of the job planning meetings and was only

briefed by the radiation protection technician who performed the ALARAjob planning.

The inspectors commented that not involving the radiation protection supervisor who was

responsible for approving a potential high radiological risk radiation work permit could

lead to the permit being approved without a complete understanding of the task. The

radiation protection and station managers acknowledged the inspectors'omment

and

stated that they would review the process of approving radiation work permits.

From interviews with the personnel involved and a review of the radiation work permit

and ALARAprejob briefing, the inspectors determined that the personnel involved knew

the radiological conditions in the area and their response to unexpected radiological

conditions.

It was also noted that each person carried an alarming, electronic dosimeter

~

~

-15-

for monitoring their accumulative dose and area dose rate.

These measures,

coupled

with the immediate actions taken to leave the room when the TIP drive began to move,

significant!y reduced the likelihood of an overexposure.

The inspectors'eview of the station's procedures,

GEN-RPP-01 "ALARAPROGRAM

DESCRIPTION," Revision 1, 11.2.2.5, "ALARAJOB PLANNINGAND REVIEWS,"

Revision 7, and 11.2.2.11, "EXPOSURE EVALUATIONSFOR MAINTAININGTEDE

ALARA,"Revision 2, identified that these procedures did not discuss management's

expectations and requirements for involving second and/or third line radiation protection

supervision in the review of high radiological risk jobs. The radiation protection and plant

managers also noted that they had identified this issue as an area of improvement and

would review their program to clearly involve second and/or third!ine radiation protection

supervision in the ALARAreview process for certain high risk radiological tasks.

C.

g~o~l<jiin

Engineering controls placed upon the traversing in-core probe Drive C were insufficient

in preventing movement of the probe during troubleshooting activities. The unexpected

movement of the probe required personnel action to prevent the probe from withdrawing

from its shielded location and into the area where the troubleshooting was being

performed.

Based upon other barriers to personnel overexposure that were in place, and

the immediate actions taken in response to the event, the likelihood of a significant

overexposure was low.

The licensee's analysis and root cause evaluation of the unexpected movement of the

traversing in-core probe accurately characterized the event and identified a number of

areas for improvement, including personnel level of knowledge of TIP system operation

and level of involvement of radiation protection supervision in the ALARAplanning

process for high radiological risk jobs.

V. I@an'a

ement Nleetin s

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee management

after the

conclusion of the inspection on February 9, 1998. The licensee acknowledged the findings

presented.

The inspectors asked the licensee whether any materials examined during the inspection. should

be considered proprietary.

No proprietary information was identified.

Supplemental Information

PARTIALLIST OF PERSONS CONTACTED

~L'se .

P. Bemis, Vice President for Nuclear Operations

F. Diya, Engineering Programs Manager

D. Hillyer, Radiation Protection Manager

P. Inserra, Licensing Manager

A. Langdon, Assistant Operations Manager

E. Neasham,

Reactor Engineering

G. Smith, Plant General Manager

R. Webring, Vice President Operations'upport

J. Weers, System Engineer

INSPECTION PROCEDURES USED

IP 37551:

IP 61726:

IP 62707:

IP 71707:

IP 71750:

IP 92901:

IP 92902:

'P

92903:

Onsite Engineering

Surveillance Observations

Maintenance Observations

Plant Operations

Plant Support

Followup - Operations

Followup - Maintenance

Followup - Engineering

Qgy~n

ITEMS OPENED, CLOSED, AND DISCUSSED

50-397/97020-01

NCV

inappropriate opening of the SM-3 PT fuse compartment

50-397/97020-02

NCV

failure of the electricians to read and adhere to the instructions on

the supply breaker's caution tag

50-397/97020-03

NCV

failure of plant procedures and instructions to control the

.configuration of the vital 4160V switchgear to ensure that its

seismic qualification was maintained

50-397/97020-04

NCV

failure of the RBMs to be operable prior to exceeding thermal

power levels of 30 percent

-2-

50-397/97020-05

NCV

failure to set the flow switches to isolate RWCU prior to exceeding

a blowdown flow of 271.1 gpm

50-397/97020-06

NCV

failure to update the FSAR

50-397/97020-07

IFI

effectiveness of the licensee's FSAR upgrade program

50-397/97020-08

VIO

inadequate labeling ofradioactive material

Qllgyd

50-397/96002-01

50-397/96003-02

VIO

inadequate troubleshooting procedures for EDG HVAC

VIO

failure to draw a reactor coolant chemistry sample within 2-6 hours

following a power change of greater than 15 percent

50-397/96003-04

IFI

failure to update the Final Safety Analysis Report

50-397/96006-05

IF I

lack of work instructions for maintenance/cleaning

50-397/96026-04

URI

failure of standby service water Pump 1A

50-397/96001-00

LER

inadvertent engineered safety feature actuation due to tripping

temporary power supply

50-397/96002-00

LER

inadvertent loss of power to vital bus and automatic start of

associated

EDG

50-397/96007-00

LER

electrical breakers not seismically qualified in test/disconnect

position

50-397/97001-00

LER

RWCU blowdown flow isolation setpoint above TS allowable

50-397/97002-00

50-397/97018-05

LER

rod block monitor calibration values not in accordance with

Technical Specifications

IFI

review of transient hydraulic loads on standby service water loop

piping

50-397/97020-01

NCV

inappropriate opening of the SM-3 PT fuse compartment

50-397/97020-02

NCV

failure of the electricians to read and adhere to the instructions on

the supply breaker's caution tag

-3-

50-397/97020-03

50-397/97020-04

NCV

failure of plant procedures and instructions to control the

configuration of the vital 4160V switchgear to ensure that its

seismic qualification was maintained

NCV

failure of the RBMs to be operable prior to exceeding thermal

power levels of 30 percent

50-397/97020-05

NCV

failure to set the flow switches to isolate RWCU prior to exceeding

a blowdown flowof 271.1 gpm

50-397/97020-06

NCV

failure to update the FSAR

LIST OF ACRONYMS USED

ALARA

DG

EDG

EO

ESF

FSAR

HVAC

IEEE

IFI

LER'RC

Ol

PER

PPM

PT

RBM

RWCU

SCBA"

SLC

TAG

TIP

TS

URI

WNP-2

as low as reasonably achievable

diesel generator

emergency diesel generator

equipment operator

engineered safety feature

Final Safety Analysis Report

heating, ventilation, and air conditioning

electrical standard

inspection followup item

licensee event report

U.S. Nuclear Regulatory Commission

. operating instruction

problem evaluation request

Plant Procedures

Manual

potential transformer

rod block monitoring

reactor water cleanup

self contained breathing apparatus

standby liquid control

training advisory group

traversing in-core probe

Technical Specifications

unresolved item

Washington Nuclear Project-2

Ir.