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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17292B7421999-07-20020 July 1999 LER 99-001-00:on 990628,ESF Signal Closed All Eight MSIVs While Plant Was Shutdown.Caused by Failure of Relay RPS-RLY-K10D.Subject Relay Was Replaced & Tested on 990630. with 990720 Ltr ML17292B4451998-10-27027 October 1998 LER 98-012-01:on 980715,failure to Comply with Requirements of TS SR 3.8.4.7 Was Noted.Caused by Inadequate Work Practices.Training Session Was Held with Personnel.With 981027 Ltr ML17284A7561998-09-0303 September 1998 LER 98-013-00:on 980805,ESF Actuations Were Noted Due to Deenergization of Vital Electrical Bus SM-8.Caused by Inadequate Direction in Troubleshooting Plan.Will Conduct Training for Engineering Personnel.With 980903 Ltr ML17284A7571998-09-0202 September 1998 LER 98-014-00:on 980807,completion of TS 3.8.1.F Required Shutdown Due to Inoperability of EDG-2 Was Noted.Caused by Degraded Voltage Regulator for DG-2.Replaced Voltage Regulator & Associated Scrs.With 980902 Ltr ML17284A7551998-09-0202 September 1998 LER 98-015-00:on 980808,discovered Reactor Coolant Pressure Boundary Leak During Shutdown Conditions.Caused by Leakage from Socket Weld (Fwb 63) on Elbow Connection.Failed Piping Connection Was Replaced.With 980902 Ltr ML17284A7311998-08-17017 August 1998 LER 98-012-00:on 980716,determined That 24-month SR 3.8.4.7 Had Not Been Fulfilled within Specified Frequency.Caused by Inadequate Work Practices.License Requested & Received Enforcement Discretion Re Battery Svc test.W/980817 Ltr ML17284A7121998-07-23023 July 1998 LER 98-006-01:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of 10CFR50,App R Calculations for High Impedance Faults.Caused by Inadequate Work Practices.Implemented Procedural Changes ML17284A6951998-07-17017 July 1998 LER 98-011-00:on 980617,ECCS Pump Room Flooding Was Noted Due to FP Sys Pipe Break.Caused by Inadequate Design of FP Sys.Detailed Review of FP Sys Design Was Conducted. W/980717 Ltr ML17284A6961998-07-15015 July 1998 LER 98-010-00:on 980615,TS Required Shutdown Due to Inoperability of TIP Sys Isolation Valve Was Noted.Caused by Improper Installation of TIP Tubing.Reattached Affected Tubing & Inspected Other TIP tubing.W/980715 Ltr ML17284A6731998-07-0101 July 1998 LER 98-009-00:on 980606,nuclear Steam Supply Shutoff Sys Group 3 & 4 Isolations During Testing Was Noted.Caused by Procedural Deficiency.Counseled Individuals Involved in preparation.W/980701 Ltr ML17284A6651998-06-24024 June 1998 LER 98-007-00:on 980530,inadvertent Full Scram & Division 1 ECCS Injection Was Noted.Caused by Failure to Meet Mgt Work Practice Expectation When Encountering Deficient Procedure. Incident Review Board Convened to Review event.W/980624 Ltr ML17284A6641998-06-24024 June 1998 LER 98-008-00:on 980531,inadvertent Full Scram During RPV Leak Testing in Mode 4 Was Noted.Caused by Change in Mgt Techniques.Revised Procedures to Take Into Account Addl Water Head in Pressure Sensing lines.W/980624 Ltr ML17284A6631998-06-19019 June 1998 LER 98-006-00:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of App R Calculations for High Impedance Fault Analysis.Caused Indeterminate. Implemented Procedural Changes Involving Operator Action ML17284A6551998-06-0404 June 1998 LER 98-005-00:on 980506,potential for Failure of RHR Sys Valve to Close on Isolation Signal Was Noted.Caused by Design Deficiency.Caution Tag Was Placed on RHR-V-40 Control Switch to Inform Plant Operators of limitation.W/980604 Ltr ML17284A6421998-06-0101 June 1998 LER 98-004-00:on 980502,determined That Primary Containment Penetration Overcurrent Protection Does Not Meet Reg Guide 1.63 Requirements.Caused by Inadequate Design Changes. Installed Addl Fuse in RHR-MO-9 circuit.W/980601 Ltr ML17292B3281998-04-0909 April 1998 LER 98-002-00:on 980311,reactor Scram & Plant Transient Occurred,Due to Failed Closed Main Steam Isolation Valve. Caused by Loss of Pneumatic Actuating Supply Pressure. Problem Evaluation Request Written for Failure of MS-V-22D ML17292B3291998-04-0909 April 1998 LER 98-003-00:on 980311,WNP-2 Experienced SCRAM Signal as Result of Low Rpv.Caused by Less than post-SCRAM Operational Strategy for Resetting SCRAM Signal in Conditions.Changes in post-SCRAM Operational Strategy implemented.W/980409 Ltr ML17292B2661998-03-0404 March 1998 LER 98-001-00:on 980203,automatic Start of HPCS EDG Was Noted.Caused by Operator Error.Operations Crew Stabilized Plant at Approximately 75% Reactor Power & Investigation of Event Was initiated.W/980304 Ltr ML17292B1111997-11-10010 November 1997 LER 97-011-00:on 971010,HPCS Battery Charger Failed.Caused by Failure of a Phase Firing Control Circuit Board Due to Aging During 7 Yrs of Use.Hpcs Sys Was Immediately Declared inoperable.W/971110 Ltr ML17292B1151997-11-0707 November 1997 LER 97-010-00:on 970906,discovered That TS SR 3.4.5.1 for Identified Portion of RCS Total Leakage Would Not Be Able to Perform within Time Limits of SR 3.0.2.Caused by Inadequate Methods.Method of Meeting SR 3.4.5.1 Established ML17292B0641997-09-24024 September 1997 LER 97-004-01:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Indication of Entry Into Region a of power-to-flow Map.Caused by Inadequate Attention to Detail.Established Event Evaluation teams.W/970924 Ltr ML17292B0241997-08-18018 August 1997 LER 97-009-00:on 970717,discovered Error in Recently Performed Inservice Testing procedure,OSP-TIP/IST-R701. Caused by Procedure Inadequacy.Plant Procedure OSP/TIP/IST-R701 Will Be changed.W/970818 Ltr ML17292B0291997-08-15015 August 1997 LER 97-008-00:on 970716,wire Seal Used to Lock Containment Instrument Air Pressure Control valve,CIA-PCV-2B,found Not Intact.Cause of Misadjustment of CIA-PCV-2B Unknown.Event Will Be Communicated to Plant employees.W/970815 Ltr ML17292B0201997-08-15015 August 1997 LER 97-S01-00:on 970718,failure to Take Compensatory Measure for Inoperative Microwave Security Zone Occurred. Caused by Personnel Error.Training Will Be Conducted W/ Appropriate Members of Security force.W/970815 Ltr ML17292A9481997-07-23023 July 1997 LER 97-007-00:on 970611,voluntary Rept of Automatic Start of DG-1 & DG-2 Was Experienced.Caused by Undervoltage Condition on Electrical Busses SM-7 & SM-8.Circulating Water Pump CW-P-1C Control Switch Placed in pull-to-lock.W/970723 Ltr ML17292A9201997-06-26026 June 1997 LER 97-006-00:on 970527,non-performance of Surveillance Requirement 3.6.1.3.2 for Blind Fanges,Was Noted.Caused Because Misunderstanding of Intent of Specs.Added Five Structural Assemblies for SP.W/970626 Ltr ML17292A8331997-04-28028 April 1997 LER 97-004-00:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Entry Into Region a of power-to-flow Map Following Planned Trip of Single Mfp. Event Evaluation teams,established.W/970428 Ltr ML17292A8311997-04-28028 April 1997 LER 97-005-00:on 970327,valid Reactor Scram Signal Received Due to Low Water Level Condition During Preparations for SRV Testing.Caused by Risks & Consequences of Decisions Not Completely Identified.Restored Water level.W/970428 Ltr ML17292A8251997-04-21021 April 1997 LER 97-003-00:on 970320,notification of Noncompliance W/Ts as TS SRs for Response Time Testing Were Not Being Met for Specified Instrumentation in Rps,Pcis & Eccs.Requested Enforcement Discretion for One Time exemption.W/970421 Ltr ML17292A7431997-03-20020 March 1997 LER 97-002-00:on 970218,determined That Rod Block Monitor (RBM) Calibr Values Were Not Set IAW Tech Specs.Caused by Calibr Procedures Inadequacies.Revised & re-performed RBM Channel Calibr procedures.W/970330 Ltr ML17292A7401997-03-13013 March 1997 LER 97-001-00:on 970211,reactor Water Cleanup Sys Blowdown Flow Isolation Setpoint Was Slightly Above TS Allowable Valve Occurred Due to Calculation Error.Lds Fss LD-FS-15 LD-FS-16 Were Declared inoperable.W/970313 Ltr ML17292A6641997-01-22022 January 1997 LER 96-009-00:on 961220,miscalculation of Instantaneous Overcurrent Relay Settings Resulted in Inoperability of safety-related Equipment.Caused by Utilization of Inappropriate Design.Testing Was completed.W/970122 Ltr ML17292A6461997-01-0606 January 1997 LER 96-008-00:on 961205,failure to Comply with TS Action Requirement for Emergency Core Cooling Sys Actuation Instrumentation Occurred Due to Unidentified Inoperability Condition.Pmr initiated.W/970106 Ltr ML17292A6371996-12-19019 December 1996 LER 96-007-00:on 961122,electrical Breakers Were Not Seismically Qualified in Test/Disconnect Position.Circuit Breaker Mfg Did Not Consider Raced Out Breaker Position During Testing.Relocated Circuit breakers.W/961217 Ltr ML17292A4121996-08-0808 August 1996 LER 96-006-00:on 960709,average Power Range Monitor Rod Block Downscale Surveillance Not Performed Prior to Entry Into Mode 1.Caused by long-standing Misinterpretation of Requirements of Tss.Procedures revised.W/960808 Ltr ML17292A3801996-07-24024 July 1996 LER 96-004-00:on 960624,plant Was Manually Scrammed by Control Room Personnel Due to Reactor Water Level Transient Experienced During Testing of Digital Feedwater Sys.Caused by Programming Error.Sys Was corrected.W/960724 Ltr ML17292A3771996-07-24024 July 1996 LER 96-005-00:on 960624,determined Missed Surveillance Test Re Channel Check of Average Power Range Monitor.Caused by Inadequate Procedures.Revised Surveillance Procedure Re When APRM Checks Must Be performed.W/960724 Ltr ML17292A3641996-07-12012 July 1996 LER 96-003-00:on 960615,required Surveillance Test Not Performed When Required by TS 3.4.1.3.Caused by Inadequate Procedures.Implementing Surveillance Procedure & Reactor Plant Startup Procedures revised.W/960712 Ltr ML17292A3361996-06-20020 June 1996 LER 96-002-00:on 960504,critical Bus SM-8 Lost Power When Supply Breaker 3-8 Tripped.Caused by Personnel Error. Operators Counselled & Procedures revised.W/960620 Ltr ML17292A2861996-05-24024 May 1996 LER 96-001-00:on 960425,inadvertent ESF Actuations Occurred Due to Tripping of Temporary Power Supply to IN-3.Caused by Personnel Error.Operations Restored to IN-3 Loads & Reset ESF actuations.W/960524 Ltr ML17291B0891995-10-19019 October 1995 LER 95-011-00:on 950919,failed to Comply W/Ts SR for RCIC Sys Due to Analysis Deficiency That Resulted in Inadequate Surveillance Test Procedure.Surveillance Procedure Revised to Correct deficiency.W/951019 Ltr ML17291A9021995-07-0707 July 1995 LER 95-010-00:on 950609,HPCS DG Declared Inoperable Due to Discovery That TS Test Method Incomplete.Caused by Inadequate Testing Procedure.Test Procedure for HPCS DG Reviewed & Special Test Procedures written.W/950707 Ltr ML17291A9031995-07-0707 July 1995 LER 95-009-00:on 950607,inadvertent MSIV Closure Occurred During Surveillance Test Due to Poor Communication Between Test Team.Determined That MSIV Closure Not Valid Because Closure Not Triggered by Plant conditions.W/950707 Ltr ML17291A8501995-06-0808 June 1995 LER 95-006-01:on 950405,reactor Scram Occurred During Surveillance Testing Due to Protective Sys Relay Failure. Replaced Failed Relay Before Plant Startup ML17291A8101995-05-12012 May 1995 LER 95-008-00:on 940125,TS Wording Lead to Potential TS Violation.Caused by Lack of Clarity in Ts.Submitted Improved TS for Plant to Provide Addl clarity.W/950512 Ltr ML17291A7841995-05-0505 May 1995 LER 95-007-00:on 950222,emergency Diesel Start Occurred Due to Voltage Transient on BPA Grid.Confirmation Was Received at 17:51 H That Disturbance Had Originated in BPA Grid ML17291A7801995-05-0404 May 1995 LER 95-006-00:on 950405,main Turbine Trip Occurred During Performance of Surveillance Test Due to Protective Sys Relay Failed.Replaced Failed Relay Before Plant startup.W/950504 Ltr ML17291A7851995-05-0303 May 1995 LER 95-005-00:on 950222,inoperable IRM Had Been Relied Upon to Meet TS Requirements During Reactor Startup.Caused by Lack of Neutron Source to Test Instrumentation. Sys Knowledge Gained Will Be incorporated.W/950503 Ltr ML17291A7071995-03-25025 March 1995 LER 95-004-00:on 950226,malfunction in Main Turbine DEH Control Sys Caused All Four High Pressure Turbine Governor Valves to Rapidly Close.Caused by Blown Fuse.Suspected Faulty Circuit Card replaced.W/950325 Ltr ML17291A7011995-03-20020 March 1995 LER 95-002-00:on 950218,automatic Reactor Scram Occurred. Caused by Erroneous Positioning of Control During Performance of Scheduled Periodic Functional Test.Control repositioned.W/950320 Ltr 1999-07-20
[Table view] Category:RO)
MONTHYEARML17292B7421999-07-20020 July 1999 LER 99-001-00:on 990628,ESF Signal Closed All Eight MSIVs While Plant Was Shutdown.Caused by Failure of Relay RPS-RLY-K10D.Subject Relay Was Replaced & Tested on 990630. with 990720 Ltr ML17292B4451998-10-27027 October 1998 LER 98-012-01:on 980715,failure to Comply with Requirements of TS SR 3.8.4.7 Was Noted.Caused by Inadequate Work Practices.Training Session Was Held with Personnel.With 981027 Ltr ML17284A7561998-09-0303 September 1998 LER 98-013-00:on 980805,ESF Actuations Were Noted Due to Deenergization of Vital Electrical Bus SM-8.Caused by Inadequate Direction in Troubleshooting Plan.Will Conduct Training for Engineering Personnel.With 980903 Ltr ML17284A7571998-09-0202 September 1998 LER 98-014-00:on 980807,completion of TS 3.8.1.F Required Shutdown Due to Inoperability of EDG-2 Was Noted.Caused by Degraded Voltage Regulator for DG-2.Replaced Voltage Regulator & Associated Scrs.With 980902 Ltr ML17284A7551998-09-0202 September 1998 LER 98-015-00:on 980808,discovered Reactor Coolant Pressure Boundary Leak During Shutdown Conditions.Caused by Leakage from Socket Weld (Fwb 63) on Elbow Connection.Failed Piping Connection Was Replaced.With 980902 Ltr ML17284A7311998-08-17017 August 1998 LER 98-012-00:on 980716,determined That 24-month SR 3.8.4.7 Had Not Been Fulfilled within Specified Frequency.Caused by Inadequate Work Practices.License Requested & Received Enforcement Discretion Re Battery Svc test.W/980817 Ltr ML17284A7121998-07-23023 July 1998 LER 98-006-01:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of 10CFR50,App R Calculations for High Impedance Faults.Caused by Inadequate Work Practices.Implemented Procedural Changes ML17284A6951998-07-17017 July 1998 LER 98-011-00:on 980617,ECCS Pump Room Flooding Was Noted Due to FP Sys Pipe Break.Caused by Inadequate Design of FP Sys.Detailed Review of FP Sys Design Was Conducted. W/980717 Ltr ML17284A6961998-07-15015 July 1998 LER 98-010-00:on 980615,TS Required Shutdown Due to Inoperability of TIP Sys Isolation Valve Was Noted.Caused by Improper Installation of TIP Tubing.Reattached Affected Tubing & Inspected Other TIP tubing.W/980715 Ltr ML17284A6731998-07-0101 July 1998 LER 98-009-00:on 980606,nuclear Steam Supply Shutoff Sys Group 3 & 4 Isolations During Testing Was Noted.Caused by Procedural Deficiency.Counseled Individuals Involved in preparation.W/980701 Ltr ML17284A6651998-06-24024 June 1998 LER 98-007-00:on 980530,inadvertent Full Scram & Division 1 ECCS Injection Was Noted.Caused by Failure to Meet Mgt Work Practice Expectation When Encountering Deficient Procedure. Incident Review Board Convened to Review event.W/980624 Ltr ML17284A6641998-06-24024 June 1998 LER 98-008-00:on 980531,inadvertent Full Scram During RPV Leak Testing in Mode 4 Was Noted.Caused by Change in Mgt Techniques.Revised Procedures to Take Into Account Addl Water Head in Pressure Sensing lines.W/980624 Ltr ML17284A6631998-06-19019 June 1998 LER 98-006-00:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of App R Calculations for High Impedance Fault Analysis.Caused Indeterminate. Implemented Procedural Changes Involving Operator Action ML17284A6551998-06-0404 June 1998 LER 98-005-00:on 980506,potential for Failure of RHR Sys Valve to Close on Isolation Signal Was Noted.Caused by Design Deficiency.Caution Tag Was Placed on RHR-V-40 Control Switch to Inform Plant Operators of limitation.W/980604 Ltr ML17284A6421998-06-0101 June 1998 LER 98-004-00:on 980502,determined That Primary Containment Penetration Overcurrent Protection Does Not Meet Reg Guide 1.63 Requirements.Caused by Inadequate Design Changes. Installed Addl Fuse in RHR-MO-9 circuit.W/980601 Ltr ML17292B3281998-04-0909 April 1998 LER 98-002-00:on 980311,reactor Scram & Plant Transient Occurred,Due to Failed Closed Main Steam Isolation Valve. Caused by Loss of Pneumatic Actuating Supply Pressure. Problem Evaluation Request Written for Failure of MS-V-22D ML17292B3291998-04-0909 April 1998 LER 98-003-00:on 980311,WNP-2 Experienced SCRAM Signal as Result of Low Rpv.Caused by Less than post-SCRAM Operational Strategy for Resetting SCRAM Signal in Conditions.Changes in post-SCRAM Operational Strategy implemented.W/980409 Ltr ML17292B2661998-03-0404 March 1998 LER 98-001-00:on 980203,automatic Start of HPCS EDG Was Noted.Caused by Operator Error.Operations Crew Stabilized Plant at Approximately 75% Reactor Power & Investigation of Event Was initiated.W/980304 Ltr ML17292B1111997-11-10010 November 1997 LER 97-011-00:on 971010,HPCS Battery Charger Failed.Caused by Failure of a Phase Firing Control Circuit Board Due to Aging During 7 Yrs of Use.Hpcs Sys Was Immediately Declared inoperable.W/971110 Ltr ML17292B1151997-11-0707 November 1997 LER 97-010-00:on 970906,discovered That TS SR 3.4.5.1 for Identified Portion of RCS Total Leakage Would Not Be Able to Perform within Time Limits of SR 3.0.2.Caused by Inadequate Methods.Method of Meeting SR 3.4.5.1 Established ML17292B0641997-09-24024 September 1997 LER 97-004-01:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Indication of Entry Into Region a of power-to-flow Map.Caused by Inadequate Attention to Detail.Established Event Evaluation teams.W/970924 Ltr ML17292B0241997-08-18018 August 1997 LER 97-009-00:on 970717,discovered Error in Recently Performed Inservice Testing procedure,OSP-TIP/IST-R701. Caused by Procedure Inadequacy.Plant Procedure OSP/TIP/IST-R701 Will Be changed.W/970818 Ltr ML17292B0291997-08-15015 August 1997 LER 97-008-00:on 970716,wire Seal Used to Lock Containment Instrument Air Pressure Control valve,CIA-PCV-2B,found Not Intact.Cause of Misadjustment of CIA-PCV-2B Unknown.Event Will Be Communicated to Plant employees.W/970815 Ltr ML17292B0201997-08-15015 August 1997 LER 97-S01-00:on 970718,failure to Take Compensatory Measure for Inoperative Microwave Security Zone Occurred. Caused by Personnel Error.Training Will Be Conducted W/ Appropriate Members of Security force.W/970815 Ltr ML17292A9481997-07-23023 July 1997 LER 97-007-00:on 970611,voluntary Rept of Automatic Start of DG-1 & DG-2 Was Experienced.Caused by Undervoltage Condition on Electrical Busses SM-7 & SM-8.Circulating Water Pump CW-P-1C Control Switch Placed in pull-to-lock.W/970723 Ltr ML17292A9201997-06-26026 June 1997 LER 97-006-00:on 970527,non-performance of Surveillance Requirement 3.6.1.3.2 for Blind Fanges,Was Noted.Caused Because Misunderstanding of Intent of Specs.Added Five Structural Assemblies for SP.W/970626 Ltr ML17292A8331997-04-28028 April 1997 LER 97-004-00:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Entry Into Region a of power-to-flow Map Following Planned Trip of Single Mfp. Event Evaluation teams,established.W/970428 Ltr ML17292A8311997-04-28028 April 1997 LER 97-005-00:on 970327,valid Reactor Scram Signal Received Due to Low Water Level Condition During Preparations for SRV Testing.Caused by Risks & Consequences of Decisions Not Completely Identified.Restored Water level.W/970428 Ltr ML17292A8251997-04-21021 April 1997 LER 97-003-00:on 970320,notification of Noncompliance W/Ts as TS SRs for Response Time Testing Were Not Being Met for Specified Instrumentation in Rps,Pcis & Eccs.Requested Enforcement Discretion for One Time exemption.W/970421 Ltr ML17292A7431997-03-20020 March 1997 LER 97-002-00:on 970218,determined That Rod Block Monitor (RBM) Calibr Values Were Not Set IAW Tech Specs.Caused by Calibr Procedures Inadequacies.Revised & re-performed RBM Channel Calibr procedures.W/970330 Ltr ML17292A7401997-03-13013 March 1997 LER 97-001-00:on 970211,reactor Water Cleanup Sys Blowdown Flow Isolation Setpoint Was Slightly Above TS Allowable Valve Occurred Due to Calculation Error.Lds Fss LD-FS-15 LD-FS-16 Were Declared inoperable.W/970313 Ltr ML17292A6641997-01-22022 January 1997 LER 96-009-00:on 961220,miscalculation of Instantaneous Overcurrent Relay Settings Resulted in Inoperability of safety-related Equipment.Caused by Utilization of Inappropriate Design.Testing Was completed.W/970122 Ltr ML17292A6461997-01-0606 January 1997 LER 96-008-00:on 961205,failure to Comply with TS Action Requirement for Emergency Core Cooling Sys Actuation Instrumentation Occurred Due to Unidentified Inoperability Condition.Pmr initiated.W/970106 Ltr ML17292A6371996-12-19019 December 1996 LER 96-007-00:on 961122,electrical Breakers Were Not Seismically Qualified in Test/Disconnect Position.Circuit Breaker Mfg Did Not Consider Raced Out Breaker Position During Testing.Relocated Circuit breakers.W/961217 Ltr ML17292A4121996-08-0808 August 1996 LER 96-006-00:on 960709,average Power Range Monitor Rod Block Downscale Surveillance Not Performed Prior to Entry Into Mode 1.Caused by long-standing Misinterpretation of Requirements of Tss.Procedures revised.W/960808 Ltr ML17292A3801996-07-24024 July 1996 LER 96-004-00:on 960624,plant Was Manually Scrammed by Control Room Personnel Due to Reactor Water Level Transient Experienced During Testing of Digital Feedwater Sys.Caused by Programming Error.Sys Was corrected.W/960724 Ltr ML17292A3771996-07-24024 July 1996 LER 96-005-00:on 960624,determined Missed Surveillance Test Re Channel Check of Average Power Range Monitor.Caused by Inadequate Procedures.Revised Surveillance Procedure Re When APRM Checks Must Be performed.W/960724 Ltr ML17292A3641996-07-12012 July 1996 LER 96-003-00:on 960615,required Surveillance Test Not Performed When Required by TS 3.4.1.3.Caused by Inadequate Procedures.Implementing Surveillance Procedure & Reactor Plant Startup Procedures revised.W/960712 Ltr ML17292A3361996-06-20020 June 1996 LER 96-002-00:on 960504,critical Bus SM-8 Lost Power When Supply Breaker 3-8 Tripped.Caused by Personnel Error. Operators Counselled & Procedures revised.W/960620 Ltr ML17292A2861996-05-24024 May 1996 LER 96-001-00:on 960425,inadvertent ESF Actuations Occurred Due to Tripping of Temporary Power Supply to IN-3.Caused by Personnel Error.Operations Restored to IN-3 Loads & Reset ESF actuations.W/960524 Ltr ML17291B0891995-10-19019 October 1995 LER 95-011-00:on 950919,failed to Comply W/Ts SR for RCIC Sys Due to Analysis Deficiency That Resulted in Inadequate Surveillance Test Procedure.Surveillance Procedure Revised to Correct deficiency.W/951019 Ltr ML17291A9021995-07-0707 July 1995 LER 95-010-00:on 950609,HPCS DG Declared Inoperable Due to Discovery That TS Test Method Incomplete.Caused by Inadequate Testing Procedure.Test Procedure for HPCS DG Reviewed & Special Test Procedures written.W/950707 Ltr ML17291A9031995-07-0707 July 1995 LER 95-009-00:on 950607,inadvertent MSIV Closure Occurred During Surveillance Test Due to Poor Communication Between Test Team.Determined That MSIV Closure Not Valid Because Closure Not Triggered by Plant conditions.W/950707 Ltr ML17291A8501995-06-0808 June 1995 LER 95-006-01:on 950405,reactor Scram Occurred During Surveillance Testing Due to Protective Sys Relay Failure. Replaced Failed Relay Before Plant Startup ML17291A8101995-05-12012 May 1995 LER 95-008-00:on 940125,TS Wording Lead to Potential TS Violation.Caused by Lack of Clarity in Ts.Submitted Improved TS for Plant to Provide Addl clarity.W/950512 Ltr ML17291A7841995-05-0505 May 1995 LER 95-007-00:on 950222,emergency Diesel Start Occurred Due to Voltage Transient on BPA Grid.Confirmation Was Received at 17:51 H That Disturbance Had Originated in BPA Grid ML17291A7801995-05-0404 May 1995 LER 95-006-00:on 950405,main Turbine Trip Occurred During Performance of Surveillance Test Due to Protective Sys Relay Failed.Replaced Failed Relay Before Plant startup.W/950504 Ltr ML17291A7851995-05-0303 May 1995 LER 95-005-00:on 950222,inoperable IRM Had Been Relied Upon to Meet TS Requirements During Reactor Startup.Caused by Lack of Neutron Source to Test Instrumentation. Sys Knowledge Gained Will Be incorporated.W/950503 Ltr ML17291A7071995-03-25025 March 1995 LER 95-004-00:on 950226,malfunction in Main Turbine DEH Control Sys Caused All Four High Pressure Turbine Governor Valves to Rapidly Close.Caused by Blown Fuse.Suspected Faulty Circuit Card replaced.W/950325 Ltr ML17291A7011995-03-20020 March 1995 LER 95-002-00:on 950218,automatic Reactor Scram Occurred. Caused by Erroneous Positioning of Control During Performance of Scheduled Periodic Functional Test.Control repositioned.W/950320 Ltr 1999-07-20
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17284A9001999-10-31031 October 1999 Rev 0 to COLR 99-15, WNP-2 Cycle 15,COLR GO2-99-177, LER 99-S01-00:on 990903,failure to Take Compensatory Measure within Required Time Upon Failure of Isolation Zone Microwave Unit,Was Noted.Caused by Personnel Error.Provided Refresher Training on Compensatory Measures.With1999-10-0101 October 1999 LER 99-S01-00:on 990903,failure to Take Compensatory Measure within Required Time Upon Failure of Isolation Zone Microwave Unit,Was Noted.Caused by Personnel Error.Provided Refresher Training on Compensatory Measures.With ML17284A8941999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for WNP-2.With 991012 Ltr ML17284A8801999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for WNP-2.With 990910 Ltr ML17284A8691999-07-31031 July 1999 Monthly Operating Rept for July 1999 for WNP-2.With 990813 Ltr ML17292B7421999-07-20020 July 1999 LER 99-001-00:on 990628,ESF Signal Closed All Eight MSIVs While Plant Was Shutdown.Caused by Failure of Relay RPS-RLY-K10D.Subject Relay Was Replaced & Tested on 990630. with 990720 Ltr ML17292B7271999-06-30030 June 1999 Monthly Operating Rept for June 1999 for WNP-2.With 990707 Ltr ML17292B6961999-05-31031 May 1999 Monthly Operating Repts for May 1999 for WNP-2.With 990608 Ltr ML17292B6641999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for WNP-2.With 990507 Ltr ML17292B6391999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for WNP-2.With 990413 Ltr ML17292B5871999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for WNP-2.With 990311 Ltr ML17292B5571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for WNP-2.With 990210 Ltr ML17292B5621999-01-31031 January 1999 Rev 1 to COLR 98-14, WNP-2 Cycle 14 Colr. ML17292B5341999-01-15015 January 1999 Part 21 Rept Re Incorrect Modeling of BWR Lower Plenum Vol in Bison.Defect Applies Only to Reload Fuel Assemblies Currently in Operation at WNP-2.BISON Code Model for WNP-2 Has Been Revised to Correct Error ML17292B5331999-01-15015 January 1999 Part 21 Rept Re XL-S96 CPR Correlation for SVEA-96 Fuel. Defect Applies Only to WNP-2,during Cycles 12,13 & 14 Operation.Evaluations of Defect Performed by ABB-CE ML17292B4791998-12-31031 December 1998 Washington Public Power Supply Sys 1998 Annual Rept. with 981215 Ltr ML17292B5351998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for WNP-2.With 990112 Ltr ML17292B5741998-12-31031 December 1998 WNP-2 1998 Annual Operating Rept. with 990225 Ltr ML17284A8231998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for WNP-2.With 981207 Ltr ML17284A8081998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for WNP-2.With 981110 Ltr ML17292B4451998-10-27027 October 1998 LER 98-012-01:on 980715,failure to Comply with Requirements of TS SR 3.8.4.7 Was Noted.Caused by Inadequate Work Practices.Training Session Was Held with Personnel.With 981027 Ltr ML17284A7831998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for WNP-2.With 981007 Ltr ML17284A7491998-09-10010 September 1998 WNP-2 Inservice Insp Summary Rept for Refueling Outage RF13 Spring,1998. ML17284A7561998-09-0303 September 1998 LER 98-013-00:on 980805,ESF Actuations Were Noted Due to Deenergization of Vital Electrical Bus SM-8.Caused by Inadequate Direction in Troubleshooting Plan.Will Conduct Training for Engineering Personnel.With 980903 Ltr ML17284A7571998-09-0202 September 1998 LER 98-014-00:on 980807,completion of TS 3.8.1.F Required Shutdown Due to Inoperability of EDG-2 Was Noted.Caused by Degraded Voltage Regulator for DG-2.Replaced Voltage Regulator & Associated Scrs.With 980902 Ltr ML17284A7551998-09-0202 September 1998 LER 98-015-00:on 980808,discovered Reactor Coolant Pressure Boundary Leak During Shutdown Conditions.Caused by Leakage from Socket Weld (Fwb 63) on Elbow Connection.Failed Piping Connection Was Replaced.With 980902 Ltr ML17284A7681998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for WNP-2.With 980915 Ltr ML17284A7311998-08-17017 August 1998 LER 98-012-00:on 980716,determined That 24-month SR 3.8.4.7 Had Not Been Fulfilled within Specified Frequency.Caused by Inadequate Work Practices.License Requested & Received Enforcement Discretion Re Battery Svc test.W/980817 Ltr ML17284A7261998-07-31031 July 1998 Monthly Operating Rept for July 1998 for WNP-2.W/980810 Ltr ML17284A7121998-07-23023 July 1998 LER 98-006-01:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of 10CFR50,App R Calculations for High Impedance Faults.Caused by Inadequate Work Practices.Implemented Procedural Changes ML17284A6951998-07-17017 July 1998 LER 98-011-00:on 980617,ECCS Pump Room Flooding Was Noted Due to FP Sys Pipe Break.Caused by Inadequate Design of FP Sys.Detailed Review of FP Sys Design Was Conducted. W/980717 Ltr ML17284A6961998-07-15015 July 1998 LER 98-010-00:on 980615,TS Required Shutdown Due to Inoperability of TIP Sys Isolation Valve Was Noted.Caused by Improper Installation of TIP Tubing.Reattached Affected Tubing & Inspected Other TIP tubing.W/980715 Ltr ML17284A6731998-07-0101 July 1998 LER 98-009-00:on 980606,nuclear Steam Supply Shutoff Sys Group 3 & 4 Isolations During Testing Was Noted.Caused by Procedural Deficiency.Counseled Individuals Involved in preparation.W/980701 Ltr ML17284A6751998-06-30030 June 1998 Ro:On 980617,flooding of RB Northeast Stairwell with Consequential Flooding of Two ECCS Pump Rooms.Caused by Inadequate Fire Protection Sys Design.Pumped Out Water from Affected Areas to Point Below Berm Areas of Pump Rooms ML17284A6641998-06-24024 June 1998 LER 98-008-00:on 980531,inadvertent Full Scram During RPV Leak Testing in Mode 4 Was Noted.Caused by Change in Mgt Techniques.Revised Procedures to Take Into Account Addl Water Head in Pressure Sensing lines.W/980624 Ltr ML17284A6651998-06-24024 June 1998 LER 98-007-00:on 980530,inadvertent Full Scram & Division 1 ECCS Injection Was Noted.Caused by Failure to Meet Mgt Work Practice Expectation When Encountering Deficient Procedure. Incident Review Board Convened to Review event.W/980624 Ltr ML17284A6631998-06-19019 June 1998 LER 98-006-00:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of App R Calculations for High Impedance Fault Analysis.Caused Indeterminate. Implemented Procedural Changes Involving Operator Action ML17284A6551998-06-0404 June 1998 LER 98-005-00:on 980506,potential for Failure of RHR Sys Valve to Close on Isolation Signal Was Noted.Caused by Design Deficiency.Caution Tag Was Placed on RHR-V-40 Control Switch to Inform Plant Operators of limitation.W/980604 Ltr ML17284A6421998-06-0101 June 1998 LER 98-004-00:on 980502,determined That Primary Containment Penetration Overcurrent Protection Does Not Meet Reg Guide 1.63 Requirements.Caused by Inadequate Design Changes. Installed Addl Fuse in RHR-MO-9 circuit.W/980601 Ltr ML17284A6491998-05-31031 May 1998 Rev 0 to COLR 98-14, WNP-2,Cycle 14 Colr. ML17292B4031998-05-31031 May 1998 Monthly Operating Rept for May 1998 for WNP-2.W/980608 Ltr ML17292B3921998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for WNP-2.W/980513 Ltr ML17292B3291998-04-0909 April 1998 LER 98-003-00:on 980311,WNP-2 Experienced SCRAM Signal as Result of Low Rpv.Caused by Less than post-SCRAM Operational Strategy for Resetting SCRAM Signal in Conditions.Changes in post-SCRAM Operational Strategy implemented.W/980409 Ltr ML17292B3281998-04-0909 April 1998 LER 98-002-00:on 980311,reactor Scram & Plant Transient Occurred,Due to Failed Closed Main Steam Isolation Valve. Caused by Loss of Pneumatic Actuating Supply Pressure. Problem Evaluation Request Written for Failure of MS-V-22D ML17292B3371998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for WNP-2.W/980409 Ltr ML17292B2641998-03-0404 March 1998 Performance Self Assessment,WNP-2. ML17292B2661998-03-0404 March 1998 LER 98-001-00:on 980203,automatic Start of HPCS EDG Was Noted.Caused by Operator Error.Operations Crew Stabilized Plant at Approximately 75% Reactor Power & Investigation of Event Was initiated.W/980304 Ltr ML17292B2911998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for WNP-2.W/980313 Ltr ML17284A7971998-02-17017 February 1998 Rev 28 to Operational QA Program Description, WPPSS-QA-004.With Proposed Rev 29 ML17292B3591998-02-12012 February 1998 WNP-2 Cycle 14 Reload Design Rept. 1999-09-30
[Table view] |
Text
.(ACCEI ERATED BIDS PROCI'.SSliG)
REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR:9410190125 DOC.DATE: 94/10/14 NOTARIZED: NO 'OCKET FACIE:50-397 WPPSS Nuclear Project, Unit 2, Washington Public Powe 05000397 AUTH. NAME AUTHOR AFFILIATION FOLEY,C.J. 'ashington Public Power Supply System PARRISH,J.V. Washington Public Power Supply System RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 94-013-02:on 940622,determined that containment isolation provisions .for both containment monitoring sys inoperable. Caused by design error. Design'hange will be implemented.W/941014 ltr.
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR / ENCL / SIZE: 7 TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
NOTES:
RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD4-2 PD 1 1 CLIFFORD,J 1 1 INTERNAL: ACRS 1 1 EOD/+OAB/DBP 2 2 AEOD/SPD/RRAB 1 1 - -LE CENTER~02 1 1 NRR/DE/EELB 1 1 NRR/DE/EMEB 1 1 NRR/DORS/OEAB 1 1 NRR/DRCH/HHFB 1 1 NRR/DRCH/HICB 1 1 NRR/DRCH/HOLB 1 1 NRR/DRSS/PRPB 2 2 NRR/DSSA/SPLB 1 1 NRR/DSSA/SRXB 1 1 NRR/PMAS/IRCB-E 1 1 RES/DSIR/EIB 1 1 RGN4 FILE 01 1 1 EXTERNAL: EG&G BRYCE,J.H 2 2 L ST LOBBY WARD 1 1 NOAC MURPHY,G.A 1 1 NOAC POORE,W. 1 1 NRC PDR 1 1 NUDOCS FULL TXT 1 1 iNOTE TO ALL"RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE iVKSTE! CONTACT TI IE DOCK'CLIENT CONTROL DESh. ROOWI PI-37 I EXT. 504. TOS3 ) TO I'.LIMINATE )'OI:R NAifL F ROTI DISTRIBUTION LISTS I'OR DOCI. MEN I'S YOL')ON"I'L'I'.D!
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 27 ENCL 27
ti WASHINGTON PUBLIC POWER SUPPLY SYSTEM P.O. Box 96B ~ 3000 George Washington Way ~ 'ichland, Washington 99352 October 14, 1994 PER 294-0602 G02-94-236 PER 294-0869 Docket No. 50-397 Document Control Desk U.S. Nuclear Regulatory Commission Washington, D.C. 20555
Subject:
NUCLEAR PLANT WNP-2, OPERATING LICENSE NPF-21 LICENSEE EVENT REPORT NO. 94-013-02 transmitted herewith is Licensee Event Report No. 94-013-02 for the WNP-2 Plant.
LER 94-013-00 reported a design deficiency in the containment isolation logic for the Containment Monitoring System (CMS). As part of the associated corrective actions, a detailed review of other containment isolation logics was performed to verify acceptable design. The subject LER revision reports a similar design deficiency discovered during this review. It should be noted that the review is complete as of this writing and no other such deficiencies were identified.
Should you have any questions or desire additional information, please call me or D.A. Swank at (509) 377-4563.
Sincerely,
. Parrish (Mail Drop 1023) sistant Managing Director, Operations JVP/CJF/my Enclosure CC: LJ Callan, NRC-RIV KE Perkins, Jr., NRC RIV, Walnut Creek Field Office NS Reynolds, Winston & Strawn NRC Sr. Resident Inspector (Mail Drop 927N, 2 Copies)
INPO Records Center - Atlanta, GA DL Williams, BPA (Mail Drop 399) 9410190125 'P41014 g~pYP PDP. ADOCK 05000:97 PDF't S
LICENSEE EVE@REPORT (LER)
AGILITY NAME (I) DOCKET NUMB R ( ) PAGE (3)
Washin ton Nuclear Plant - Unit 2 0 5 0 0 0 3 9 7 I DF ITLE (4)
DESIGN ERROR IN ELECTRICAL CIRCUITRY FOR CONTAINMENT ISOLATION EVENT DATE (5) LER NUMBER ( REPORT DATE 7 OTHER FACILITIES INVOLVED (8 MONTH DAY YEAR YEAR SEQUENTIAL EVI 5 ION MONTH DAY YEAR FACILITY NAMES CKE UMB R (5)
NUMBER UMBER 050 0 6 2 2 94 9 4 0 1 3 0 2 I 0 1 4 9 4 50 PERATING MIS REPORT IS SUBMITTED PURSUANT TO THE REQUIREMENTS OF 10 CFR II: (Ch eck one or more of the fo llowing) (11)
ODE (9)
O'NER LEVEL 20.402(b) 0.405(C) 0.73(a)(2)(iv) 77.71(b)
'10) =
0.405(a)(1)(i) 0.36(c) 1) X 0.73(a)(2)(v) 73.73(c) 0.405(a)(1)(ii) 50.36(c) 2) 50.73(a)(2)(vii) THER (Specify in Abstract 0.405(a)(1)(iii) 0.73(a) 2)(i) 50.73(a)(2)(viii)(A) elow and in Text, HRC 0.405(a)(1)(iv) 50.73(a) 2)(ii) 50.73(a)(2)(viii)(B) Form 366A) 20.405(a)(1)(v) 50.73(a)(2)(iii) 50.73(a)(2)(x)
LICENSEE CONTACT FOR THIS LER (12)
TELEPHOHE NUMBER REA CODE C.J. Foley, Licensing Engineer 5 0 9 7 7 - 4 3 2 5 COMPLETE ONE LIHE FOR EACH COMPOHEHT FAILURE DESCRIBED IH THIS REPORT (13)
CAUSE SYSTEM COMPONENT MANUFACTURER EPORTABLE CAUSE SYSTEM COMPONENT MANUFACTURER REPORTABLE 0 NPRDS TO NPRDS NA NA SUPPLEMEH1'AL REPORT EXPECTED (14) EXPECTED SUBMISSION MONTH DAY YEAR ATE (15)
YES (If yes, complete EXPECTED SUBMISSIOH DATE) HO TIIACT nd)
On June 22, 1994, it was determined that containment isolation provisions for both Containment Monitoring Systems were inoperable because the design of the electrical circuitry was such that failure of a single electrical relay could prevent closure of the solenoid-operated containment isolation valves associated with those particular systems. The plant was in an annual refueling and maintenance outage.
The root cause is design error during initial plant construction. A plant modification was executed to revise the electrical circuitry to eliminate the design fiaw causing the deficiency. In addition, a detailed review of the logic circuits for the other electrically powered isolation valves listed in Technical Specification 3.6.3 was performed. One other case was discovered in which failure of a single relay could prevent closure of solenoid-operated containment isolation valves associated with the hydraulic control system for the two fiow control valves for the Reactor Recirculation System. A request for enforcement discretion and an emergency Technical Specifications Amendment was processed to allow continued operation until the next shutdown at which time a modification will be implemented to eliminate the design fiaw causing the deficiency,
LICENSEE EVENT REPORT (4)
TEXT CONTINUATION ACILITY NAME (1) OOCKET NUHBER (2) LER NUHBER (8) AGE (3)
Year umber ev. No.
. Washington Nuclear Plant - Unit 2 0 5 0 0 0 3 9 7 4 13 02 2 OF 6 ITLE (4)
DESIGN ERROR IN ELECTRICAL CIRCUITRY FOR CONTAINMENT ISOLATION Even De cri tion There are two cases of the same type of event, as follows:
Case No. 1 On June 22, 1994, the plant was in operational condition 5 (refueling) at 0% power. An electrical engineer, evaluating a report provided'by INPO about a condition discovered at another nuclear plant, determined that a single failure of an electrical relay [RLYJ used in containment isolation logic circuits [JM] could prevent closure of solenoid-operated containment isolation valves [ISV] for the WNP-2 Containment Monitoring System [D]
(CMS). The NRC was immediately notified per 10CFR50.72(b)(1)(ii)(B) because this condition was a violation of the single-failure criterion.
Case No. 2 On September 15, 1994, the plant was in operational condition l,at 100% power. An electrical engineer discovered that a single failure of an electrical relay used in containment isolation logic circuits [JM] could prevent closure of solenoid operated containment isolation valves [ISV] for the hydraulic system used to control the position of the Qow control valves [FCV] of the Reactor Recirculation System [AD]. The NRC was immediately notified per 10CFR50.72(b)(i)(ii)(B) because this condition was a violation of the single failure criterion.
Immediate orrective Action For the first case, the Containment Monitoring System was declared inoperable on June 22, 1994. For the second case, the isolation valves for the Reactor Recirculation System Valve Positioning System were declared inoperable on September 15, 1994.
Fu her Evaluati n Case No. 1 Two Containment Monitoring Systems serve as reactor coolant pressure boundary [AD] leak detection systems in conformance with Regulatory Guide 1.45. The closed loop systems, installed in cabinets located in the secondary containment area, draw samples of primary containment [NH] atmosphere through radiation monitors [MON],
arid return the samples to the primary containment. Containment isolation valves are provided for each system pursuant to GDC 56 as follows: 1) two solenoid-operated valves located outside of primary containment are installed in series in the sample supply line, and 2) a single solenoid-operated valve located outside of containment plus a check valve located inside containment provides isolation for the sample return line.
LICENSEE EVENT REPORT ('+)
TEXT CONTINUATION AGILITY NAME (1) OOCKET NUMBER (2) LER NUMBER (8) AGE (3) ear umber ev. No.
Washington Nuclear Plant - Unit 2 0 5 0 0 0 3 9 7 4 013 02 3 OF 6 ITLE (4)
DESIGN ERROR IN ELECTRICAL CIRCUITRY FOR CONTAINMENT ISOLATION The solenoid operated valves are spring-loaded to close upon interruption of power to the solenoid [SOL].
The electrical circuitry that controls the position of these valves involves a one-out-of-two "taken twice" logic requiring receipt of either a "high" drywell pressure or "low" reactor water level signal in two separate circuits to interrupt power to the solenoids to allow the valves to close. Division 1 power is used to operate the logic associated with the isolation valves for one of the monitoring systems, and Division 2 power is used for the other. Each set of three valves is controlled by two electrical relays that must change position to allow the valves to close; the two relays for each set are within a single division. With this arrangement, failure of one of the two relays in the logic could prevent closure of its associated three isolation valves, which does not satisfy the single failure criterion as applied to containment isolation.
Case No. 2 The two Reactor Recirculation (RRC) System flow control valves, located within primary containment, are positioned by separate hydraulic systems located outside of primary containment. Small bore piping transports hydraulic fluid from the hydraulic systems to the flow control valves; the interior of this piping is filled with hydraulic Quid, and is operated at a pressure of approximately 1800 psig when the RRC system is in operation.
There are eight separate hydraulic piping runs, each provided with two solenoid-operated fail-closed valves pursuant to the requirements of GDC 56, for a total of sixteen containment isolation valves; the valves are physically located outside of primary containment for environmental and maintenance reasons. The piping is designed and fabricated to ASME Section III, Seismic 1, requirements between the primary containment shell and the outer isolation valve, and to ANSI B31.1, Seismic 2+, requirements elsewhere.
The electrical circuitry that controls the position of these valves involves a one-out-of-two "taken twice" logic requiring receipt of either a "high" drywell pressure or "low" reactor water level signal in two separate circuits to interrupt power to the solenoids to allow the valves to close. Division 1 power is used to operate the logic associated with the isolation valves for one of the hydraulic systems, and Division 2 power is used for the other.
Each set of eight valves is controlled by four electrical relays that must change position to allow the valves to close; the relays for each set are within a single division. With this arrangement, failure of any of four different relays in the logic to open could prevent closure of eight isolation valves, which does not satisfy the single failure criterion as applied to containment isolation.
oot ause The root cause is design error during initial plant construction.
In Case No. 1, the original design, released in 1979, included appropriate divisional separation, and consequently was not subject to this deficiency. However, a design change in 1982 eliminated the divisional separation, thereby causing the deficiency as it existed when found. No records have been located documenting the rationale for the 1982 change.
LICENSEE EVENT REPORT (+I)
TEXT CONTINUATION AGILITY NAME (1) OOCKET NUMBER (2) LER NUMBER (8) PAGE (3)
Year Number ev. No.
Washington Nuclear Plant - Unit 2 0 5 0 0 0 3 9 7 4 013 02 4 F 6 ITLE (4)
DESIGN ERROR IN ELECTRICAL CIRCUITRY FOR CONTAINMENT ISOLATION In Case No. 2, the original design, released in 1981, was based on GDC 57 and thus had only a single containment isolation valve in each line. In the licensing process the design was changed in 1982 to conform to GDC 56 requirements. The powering arrangement for the double valves was described in the FSAR as being uni-divisional so that no single loss of power could close some isolation valves in both sets of hydraulic lines thus rendering both RRC fiow control valves inoperable. However, susceptibility to single component failure was not adequately addressed.
Further orrective Action A complete review of the design for the automatic electrically-powered containment isolation valves listed in
'Ibchnical Specification 3.6.3-1 was performed to ensure the single failure criterion was met. Only two cases were found wherein a single component failure could prevent containment isolation. These two cases are covered by this LER.
Case No. 1 The configuration of the control and indication circuitry for the solenoid-operated valves in the sample return lines was modified to eliminate the deficiency. The modification exchanged the control and indication circuits for one of the solenoid valves in each of the sample supply lines with that of the other electrical division, so that one of the two valves in series is actuated by the Division 1 logic and the other by the Division 2 logic. With this arrangement, failure of a single relay in either division's logic cannot prevent containment isolation.
Case No. 2 On September 15, 1994, WNP-2 was granted interim enforcement discretion to permit continuing operation in violation of Technical Specification 3.6.3 until an emergency Technical Specification change could be processed.
This was confirmed by the NRC in writing on September 20, 1994. On September 18, an emergency Technical Specification request was formally filed to allow continued operation to the next shutdown but not later than May 15, 1995. In this interim period the systems will be operated normally. Should an event arise calling for isolation of primary containment and should a relay failure prevent automatic closure of one or more isolation valves for the RRC hydraulic system, plant operators will manually close the valves using switches available in the Control Room. Should that be unsuccessful, the operators will pull fuses in the Control Room, thus removing all power from the isolation valves and allowing them to close.
During the next reactor shutdown, a design change will be implemented such that the two isolation valves in each line will be supplied from different logic, thus eliminating the susceptibility to single component failure.
LICENSEE EVENT REPORT OR)
TEXT CONTINUATION AGILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (8) PAGE (3)
Year Number ev. No.
Washington Nuclear Plant - Unit 2 0 5 0 0 0 3 9 7 4 013 02 5 OF 6 ITLE (4)
DESIGN ERROR IN ELECTRICAL CIRCUITRY FOR CONTAINMENT ISOLATION f i nifi n Case No. 1 The equipment and tubing tYBG] comprising the Containment Monitoring Systems is a leak-tight closed loop boundary isolating the primary containment atmosphere from secondary containment. These systems are not qualified as extensions of primary containment, but are equipped with pressure switches tPS] to isolate the sample supply and return lines from the system if the system pressure should rise to 2 psig. Leakage from the supply and return tubing or from the monitoring systems would enter the secondary containment which is designed to mitigate radioactive releases. Consequently, two barriers exist to limit the release of radioactivity in the event of a LOCA and concurrent failure of the containment isolation valves to close (the closed loop systems and secondary containment).
An existing analysis was available to assess the radiological consequences of a postulated accident involving the following assumed simultaneous failures: a LOCA involving core damage, failure of the containment isolation valves in the sample return line to close, and a breach of the closed loop system outboard of the open containment isolation valves. Based on the assumptions, the analysis showed that the 10CFR100 reference values for thyroid exposure at the exclusion boundary and GDC 19 thyroid limits for the control room would be exceeded. The assumptions included one open path from primary containment, while the deficiency described in this LER could involve two open paths which also result in exceeding 10CFR100 reference values and GDC 19 limits.
.Using figures from WNP-2 probabilistic risk studies, the probability of a LOCA with accompanying release of radioactivity to the containment atmosphere is 1.78 x 10'/year and the probability for a single relay to fail to open is 6 x 10~/year. The aggregate probability for radioactive release from primary containment is (1.78 x 10')
x (6 x 10') x 2 = 2 x 107/year; the factor of 2 is used because two relays must change position to effect containment isolation.
Case No. 2
'The'equipment and piping providing RRC valve actuation hydraulic power is a leak tight closed boundary which is normally filled with hydraulic fiuid operating at 1800 psig, Consequently, three barriers exist to limit the release of radioactivity in the event of a LOCA and concurrent failure of the containment isolation valves to close (the primary containment, the closed hydraulic piping, and the secondary containment).
Using figures from WNP-2 probabilistic risk studies, the probability of a LOCA with accompanying release of radioactivity to the primary containment is 1.78 x 10'/year and the probability for failure of a single relay to fail to open is 6 x 10'/year. Assuming for conservatism that the hydraulic piping were to fail both inside and outside of primary containment concurrent with this event, the aggregate probability for release of radioactivity to the secondary containment and then to the environment is (1.78 x 10') x (6 x 10') = 1 x 10'/year. These assumptions would yield essentially the same radiological consequences as is discussed under Case No. 1.
'ICENSEE EVENT REPORT (l)
TEXT CONTINUATION AGILITY NANE (1) OOCKET NUMBER (2) LER NUNBER (8) AGE (3)
Year umber ev. No.
Mashington Nuclear Plant - Unit 2 0,5 0 0 0 3 9 7 4 013 02 6 OF 6 ITLE (4)
DESIGN ERROR IN ELECTRICAL CIRCUITRY FOR CONTAINMENT ISOLATION Summary While neither the Containment Monitoring System nor the hydraulic piping external to the outboard isolation valves are qualified as extensions of containment, they do consist of closed loops that function as a pressure boundary during normal plant operations. The probability of failure of the pressure boundary of those systems is low, but not quantifiable, because the monitoring systems have not previously been considered in probabilistic risk studies at WNP-2. However, those boundaries do provide further reduction of the aggregate failure probabilities calculated above which are only slightly different from the 1.2 x 10'/year probability of release of radioactivity by a large LOCA to the uncontrolled environment from all events evaluated by the WNP-2 probabilistic risk analysis.
Based on the above, it is concluded that the design error involving the electrical circuitry used to control containment isolation valves for the Containment Monitoring Systems was of low safety significance.
LER 94-009 "Incorrect Isolation Valve Component Selection," reported installation of excess flow check valves as inboard isolation valves in the sample return lines for the Containment Monitoring Systems. This type of check valve was determined to be unable to satisfy requirements for the particular installation since such valves could open without operator action when primary containment pressure had dropped below approximately 3.5 psid after a LOCA. The corrective action was to replace the excess flow check valves with ordinary check valves. However, that corrective action could not have been expected to address the deficiency of this LER because it involved a passive mechanical device problem, while the present event involves an electrical design error.
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