ML17290B064

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Insp Rept 50-397/94-02 on 940110-28.Violations Noted.Major Areas Inspected:Design Changes,Temporary Plant Modifications,Engineering Involvement,Design Basis & Self Assessment
ML17290B064
Person / Time
Site: Columbia Energy Northwest icon.png
Issue date: 03/11/1994
From: Narbut P, Vandenburgh C
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML17290B062 List:
References
50-397-94-02, 50-397-94-2, NUDOCS 9403310115
Download: ML17290B064 (45)


See also: IR 05000397/1994002

Text

U.S.

NUCLEAR REGULATORY COMMISSION

REGION V

Report

No.

'0-397/94-02

.

Docket No.

50-397

License

No.

NPF-21

Licensee:

Facility Name:

Inspection at:

Inspection

Conducted:

'ashington

Public Power Supply System

P. 0.

Box 968

Richland,

WA 99352

Washington Nuclear Project

No.

2 (WNP-2)

WNP-2 site near Richland,

Washington

January

10 through 28,

1994

Inspectors:

P.

C.

W.

A.

Narbut,

Regional

Team Leader

Hyers,

Reactor

Inspector

Wagner,

Reactor

Inspector

HacDougal,

Resident

Inspector

(Palo Verde)

Contractors:

Submitted by:

H. Kister, Parameter

Inc.

S. Traiforos,

Parameter

Inc.

P.

P.

ar ut,

earn

ea er

ate

Approved by:

~Summar:

. A.

an

en urg

, Act

g

eputy

erector

Division of Reactor Safety

and Projects

a(u4+

ate

Ins ection

on Januar

10-28

1994

Re ort No. 50-397 94-02

Areas

Ins ected:

An announced,

team inspection of WNP-2 engineering

and

technical

support.

The areas

examined

were design

changes,

temporary plant

modifications,

engineering

involvement,

design bases,

engineering

capabilities,

and self-assessment

programs.

NRC Inspection

Hanual

Chapters

61726,

62703,

37700,

40500,

and

a draft inspection

procedure entitled

"Engineering

and Technical

Support" were used for guidance.

Results of Ins ection

and General

Conclusions:

The inspection

found that the

licensee

had recently implemented

several

important improvement initiatives

which appear to be having positive results.

Examples of these initiatives

included engineering

backlog reduction,

temporary modification reduction,

and

an improved interface

between

engineering

and other organizations.

The team

9403310115

940315

PDR

ADOCK 05000397

PDR

also observed that the licensee

had decided to install

new metallic-seated

containment

purge

and supply isolation valves in order to end

a longstanding

problem with leaks in the rubber-seated

valves.

Two significant unresolved

items were identified involving the adequacy of the proposed modification and

the

10 CFR 50.59 safety evaluation for the

BWR level instrumentation backfill

system;

and the presence

of flow limiting orifices, which are larger than

described

in the

FSAR, for

115 instrumentation lines penetrating

containment.

Si nificant Safet

Matters:

None.

Summar

of Violations and Deviations:

One violation was identified for the

failure to periodically verify the position of manual

containment isolation

valves in accordance

with technical specification requirements.

The involved

valves were

115 manual

bypass

valves for the containment isolation excess

flow

check valves.

No deviations

were identified.

Six open items were identified for followup.

Table of Contents

1.0

Introduction

2.0

Executive

Summary

.

3.0

Persons

Contacted

.

4.0

Examination of Design

Changes

.

.

.

.

.

.

.

.

.

.

.

.

.

.

.

.

.

.

4.1

In-Process

Modifications

4.1.1

Sample

and Criteria................

4.1.2 Findings

4. 1.2. 1

Containment Isolation Valve Replacement

4.1.2.2

Reactor

Water Level Instrumentation

Backfill Modification

.

.

.

.

.

.

.

.

.

4.1.2.3

Excess

Flow Check Valves

4. 1.2.4

Incorrect Orifice Size

4. 1.3 Conclusions

.

.

.

.

.

.

.

.

.

.

.

.

~

~

~

~

~

~

~

~

~

~

~

~

~

~

10

15

17

18

4.2

4.3

Completed Modifications

.

4.2. 1 Sample

and Criteria

4.2.2 Findings

4.2.3 Conclusions

.

.

.

.

Temporary

and Minor Modifications

.

.

4.3.1

Sample

and Criteria

.

.

.

.

.

.

.

.

.

.

.

.

.

4.3.2 Findings

4.3.2. 1

Overall

Program Review

4.3.2.2

Hain Steam Isolation Valve (HSIV)

Hodification

4.3.2.3

Disabled Control

Room Annunciator

4.3.2.4

Inadvertent

Design

Changes

4.3.3 Conclusions

.

.

.

.

.

.

.

.

. .,.

.

.

.

.

.

.

18

18

19

19

19

19

20

20

20

20

'21

23

5.0

Engineering

Involvement in Plant

Problems

.

.

.

.

.

.

.

.

.

.

.

.

23

5.1

Nonconformance

Review

.

5.1.1

Sample

and Criteria,.

5.1.2 Findings

5.1.3 Conclusions

.

~

~

~

23

23

24

24

5.2

5.3

Engineering

Involvement in the Reactor

Pressure

Vessel

(RPV)

Nozzle/Safe-End

Stress

Improvement

Process

5.2.1

Sample

and Criteria

.

5.2.2 Findings

5.2.3 Conclusions

.

.

.

.

.

.

.

.

.

.

.

.

.

.

.

.

.

.

.

.

.

Waterhammer

Incidents in the Standby Service Water System

(SSWS)

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

0

~

~

~

~

~

5.3.1

Sample

and Criteria

.

5.3.2 Findings

5.3.3 Conclusions

.

25

25

25

26

26

26

26

29

5.4

Suspected

HPCS Materhammer

Event

5.4.1

Sample

and Criteria

.

5.4.2 Findings

5.4.3 Conclusion

29

29

~

~

~"

30

30

5.5

Spray

Pond Icing

5.5. 1 Sample

and Criteria

.

5.5.2 Findings

5.5.3 Conclusions

.

.

.

.

.

~

~,

~

~

~

~

30

30

31

32

6.0

Engineering

Communications

and

Programs

.

.

.

.

.

.

6. 1

Sample

and Criteria

.

.

.

.

.

.

.

.

.

.

.

.

.

32

32

6.2

F

d

~

~

~

1 tldlngs ..

~

6.2. 1 System Engineering

Performance

6.2.2 Plant Performance

Monitoring and Trending

6.2.3 Design Engineering Effectiveness

6.2.4 Project

Management Activities .

.

.

.

.

.

6.2.5 Design Basis

Pr

~

~

~

ogram

33

33

36

38

41

41

6,3

Conclusions

.

t

7.1.1

Sample

and Criteria

.

7.1.2 Findings

7.1.3 Conclusions.....

8.0

Exit Meeting

7.0

Licensee Self Assessment

~

~

7.1

guality Assurance

Oversigh

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

~

42

44

44

44

44

45

45

1.0

Introduction

The inspection

was performed to assess

the licensee's

engineering

and

technical

support activities, particularly the effectiveness

of the

Engineering organization to perform routine

and reactive site activities,

including the identification and resolution of technical

issues

and problems.

2.0

Executive

Summary

The team inspection

was conducted

at .the

WNP-2 site for two separate

weeks.

The team consisted of a team leader,

three

NRC inspectors,

and two

contractors.

The purpose of the inspection

was to assess

the effectiveness

of engineering

and technical

support at WNP-2.

The areas

examined

were design

changes,

temporary plant modifications,

engineering

involvement, design

bases,

engineering capabilities,

and self-assessment

programs.

For inspection

samples,

important systems

and .components

were selected for examination

using

generic

and plant specific probabilistic risk assessment

(PRA) data.

The inspectors

noted that the licensee

had recently implemented

several

important improvement initiatives which appear to be having positive results.

Examples of these initiatives included engineering

backlog reduction,

temporary modification reduction,

and improved interface

between

engineering

and other organizations.

The inspectors

considered

that the licensee's

.decision to install

new metallic-seated

containment

purge

and supply isolation

valves in order to end

a longstanding

problem with leaks in the rubber-seated

valves

was commendable.

The inspectors

also noted two significant unresolved

items which suggest

additional

improve'ment

and management

attention is warranted.

The unresolved

items involved the adequacy of the proposed modification and the

10 CFR 50.59

safety evaluation for the Boiling Water Reactor

(BWR) level instrumentation

backfill system

and secondly,

the presence

of flow limiting orifices, which

are larger than described

in the Final Safety Analysis Report

(FSAR), in 115

instrumentation lines penetrating

containment.

The inspection also identified

a violation involving the failure to

periodically verify the position of manual

containment isolation valves in

accordance

with Technical Specification requirements.

The valves involved

were

115 manual

bypass

valves for the containment isolation excess

flow check

valves.

Detailed Conclusions

The inspection

concluded that completed modifications generally

appeared

to

meet regulatory requirements.

In reviewing modifications in process

the

inspection

concluded that engineering

appeared

to be actively involved.

Their

involvement

was evident in the identification and resolution of a longstanding

technical

issue involving leaking containment

supply

and exhaust isolation

valves.

The inspection also observed that engineering

had been actively

involved in the development of the reactor vessel

level indication backfill

modification.

Their activities included involvement with the Boiling Water

Reactor Owner's

Group

(BWROG) in the development of the modification as well

as close coordination with operations

and maintenance.

However, the

inspection identified an unresolved

item regarding the adequacy of the

proposed backfill modification from the standpoint of the credibility,of

initiating an unanalyzed

event through the blockage of a single

instrumentation line,

and regarding the adequacy of the licensee's

10 CFR 50.59 review and safety analysis.

Also, in conjunction with the inspector's

review of the modification, the inspection identified

a longstanding violation

involving the failure to verify that the bypass

valves for the

115 excess

flow

check valves were closed or locked in their closed position.

Additionally,

the inspection identified another longstanding

problem regarding

improper

instrument line orifice sizes.

In the review of temporary modifications,

the inspection

concluded that the

licensee

had initiated programs

which significantly improved their oversight

and management

of the temporary modification program.

For example,

the number

of temporary modifications

and the

age of the modifications

had

been

significantly reduced.

However,

some problems

we) e identified in the area of

temporary modifications.

One problem involved an inadvertent

design

change to

the Post-Accident

Sampling

System

(PASS)

caused

by closing normally-open,

manually-operated,

demineralized

water valves.

This resulted in the loss of

the ability to remotely flush portions of the

PASS to reduce

area radiation

levels.

A second

problem involved a weakness

in the administrative

procedures

for controlling valve lineup exceptions.

Improvements

were noted in the involvement of engineering

in the plant

activities.

A review of nonconformances

indicated that engineering

was

involved in the identification and resolution of technical

issues

affecting

the plant.

Likewise, engineering

was found to be involved in major plant

maintenance.

Specifically, it was observed that engineering

was actively

involved in the reactor pressure

vessel

nozzle

and safe-end

stress

improvement

process

planned for the upcoming outage.

On the other hand, the inspection

concluded that the licensee's

examination of a recurrence of waterhammer

in

the Standby Service Mater system in late

1993 was not as thorough

as would be

expected for a repetitive problem.

Additionally, the licensee's

interim

disposition of increasing

the valve stroke time was not correctly calculated

and

may have contributed to another

waterhammer

event.

However, the team

noted that engineering

involvement in an apparent

waterhammer

event in the

High Pressure

Core Spray system that occurred during the inspection

was

prompt, thorough,

and responsive

to the needs of the plant.

Engineering

assistance

was evident,

and the appropriate

degree of analysis

and root cause

determination

was performed.

The inspection

concluded that,

although

areas requiring improvement remained,

the degree

and effectiveness

of the support provided by the engineering

organizations for plant operations

was clearly improving.

This was further

evidenced

by observed

improvements

in the implementation of the licensee's

programs for personnel

and equipment

performance.

For example,

the inspection

concluded that System Engineering

appeared

to have

improved

and was poised for

'Qa

more improvement,

although certain oversights

in program definition were

observed.

Additional staff needs

were being addressed,

and interviews with

operators

indicated that System Engineering

support of plant operations

had

improved.

Also, the inspection

concluded that the licensee's

plant performance

monitoring and trending programs

could have

been better

managed.

For example,

the program administrative control

docume'nt did not address all of the various

performance monitoring activities being performed

and certain monitoring

activities were being performed without benefit of a management-approved

procedure.

The inspection also concluded that the various engineering

improvement

initiatives that were in progress

or planned

should improve the effectiveness

of engineering

support for the operation of the plant.

Specifically, the work

that had

been

done

on reducing the engineering

backlog

had already

shown

a

significant impact.

Furthermore,

the plant staff's visits to other sites with

successful

programs

appeared, to be effective in improving performance

in key

areas

such

as System Engineering.

Additionally, the licensee's

increased

involvement in external

committee activities appeared

to improve focus

on

ongoing industry initiatives.

However, the inspection

concluded that it was

too early to assess

long term effectiveness

of the engineering initiatives and

some weaknesses

were identified.

For example,

the inspection

noted that

licensee

management

had not established

an agreed

upon set of expectations

to

assure

the effectiveness

of Design Engineering interface with Operations

or

System Engineering.

Also, the inspection

found that design requirements

documents

did not contain sufficient information to make them useful to plant

users.

In addition, the validation and verification of most of the documents

was not well controlled

and resulted in varying degrees

and types of

validation and verification'.

I

4

i

3.0

Persons

Contacted

Was

  • J
  • M.
  • J
  • J
  • G
  • R.
  • H
  • J

%J

~R.

~R.

C.

  • D

J.

H.

  • W.
  • W
  • S
  • K.
  • J
  • J
  • C.
  • D
  • G
  • p
  • D

W.

Bonneville Power Administration

  • A. Rapacz
  • R. F. Mazurkiewicz

hin ton Pub1ic

Power

Su

1

S stem

V. Parrish,

Assistant

Managing Director for Operations

P. Flasch,

Engineering Director

C. Gearhart,

guality Assurance Director

H. Swailes,

Plant Manager

O. Smith, Operations

Division Hanager

L. Webring, Technical

Services

Manager

M. Nonopoli, Maintenance Division Manager

M. Benjamin, guality Assessments

Manager

R.

Sampson,

Maintenance

Production

Manager

J.

Barbee,

System Engineering

Manager

L. Koenigs,

Design Engineering

Manager

M. Whitcomb, Engineering

Management

Support

Manager

W. Coleman,

Acting Regulatory

Programs

Manager

P. Albers, Radiation Protection

Hanager

E. Kook, Jr.,

Licensing Manager

S. Davison, guality Assuran'ce,

Plant Support Assessments

D. Shaeffer,

Operations

Manager

H. Peck,

Equipment Engineering

Manager

B. Lewis, Licensing Engineer

Snyder,

Plant Support Engineer

Baker, Technical Training Manager

D. Scott, Supervisor,

Plant Support Engineering

Matthews,

Design Engineering

Myers, Design Engineering

Moore, Supervisor,

Engineering

Data Bases

J. Inserra,

Supervisor,

Technical

Services

R.

Bauman,

Executive Assistant to the Managing Director

L. Heade,

Supervisor,

Technical

Services

L. Larkin, Manager,

Engineering Services

La Frambroise,

Structural

Engineer

Manager

United States

Nuclear

Re ulator

Commission

  • P. H. Johnson,

Chief, Project Section I, Region

V

  • R. C. Barr, Senior Resident

Inspector

  • S. P.

Sanchez,

Resident

Inspector

  • D. L. Proulx, Resident

Inspector

  • T. P.

Gwynn, Director, Division of Reactor Safety,

Region

IV

  • T. F. Westerman,

Chief, Engineering

Branch,

Region

IV

+Attended the Exit Meeting on January

28,

1994.

The inspectors

also interviewed various control

room operators; shift

supervisors

and shift managers;

and maintenance,

engineering,

quality

assurance,

and management

personnel.

I

4.0

Examination of Design

Changes

4.1

In-Process

Modifications

The inspector evaluated

the extent

and quality of engineering

involvement in

modifications which were in progress

during the inspection.

In-process

modifications were selected

to assess

the effectiveness

of recent engineering

initiatives.

4.1.1

Sample

and Criteria

The inspector reviewed portions of the existing design

packages for the

following in-process

plant modifications:

~

Purchase

Order 236550-001,

Containment Isolation Valve Replacement

~

Basic Design

Change

(BDC) 93-0089,

Reactor Water Level

Instrumentation Backfill Nodification

The inspector discussed

the development of the modifications with

cognizant licensee

personnel,

reviewed the associated

procedures,

and

walked

down accessible

portions of the modified components

and systems.

4.1.2 Findings

4.1.2.1

Containment Isolation Valve Replacement

The inspector found that the containment isolation valve

modification was in the preliminary stages of design

and

procurement.

The modification affected four butterfly valves that

provide the supply

and exhaust for the primary containment

atmosphere

(CSP V-3, V-4, and

CEP V-IA, V-2A).

These valves were

normally closed during power operation with the containment

atmosphere

inerted.

However, the valves

can

be open during

certain low power operating

modes

and are required to

automatically close for containment integrity.

The licensee

had

experienced

persistent

problems in obtaining acceptable

leak test

results following repositioning of the valves during outages.

The inspector discussed

the development of the licensee's

design

and the engineering

involvement in improving the reliable sealing

of the valves.

The inspector also reviewed six problem evaluation

requests

(PERS) identifying problems related to the containment

isolation valves.

The inspector

found that engineering

had

been

involved in attempting to improve the existing butterfly valves

for a period of four years.

This effort involved improvements

in

both the design of the resilient seals

and maintenance

practices

for the installation of the seals.

While achieving

some

success

in these efforts, acceptable

valve sealing

performance

was not

sustained.

-10-

In May 1993, the licensee

found apparent

valve body distortion

which affected the valve's sealing capability.

According to the

licensee,

the distortion appeared

to have

been

induced

by valve

flange bolting.

Due to the observed

lack of rigidity of the valve

body, the licensee

abandoned

further efforts to improve the

existing equipment

and initiated the procurement of higher

reliability replacement

valves.

The inspector

reviewed

Procurement Specification

No.

12111,

Revision

1,

and Purchase

Order 236550-001 for the new butterfly

valves.

The replacement

valves consisted of cast valve bodies

with metal seals,

rather than the resilient seals.

Conclusion

The inspector

found that engineering

had been

involved in the

development of improved performance for the containment isolation

valves.

In particular,

the inspector

noted that the licensee's

decision to replace the existing butterfly valves with higher

reliability valves represented

a substantial

resource

commitment

to improve the safety-related

performance of the valves

and the

overall reliability of the unit.

4.1.2.2

Reactor

Water Level Instrumentation Backfill

Modification

The inspector

reviewed Modification BDC 93-0089

and walked down

accessible

portions of the modification, which had been partially

installed.

The modification involved the reactor vessel

water

level instrumentation.

The modification installed

a backfill

system for the reference

leg of the condensing

pots in response

to

NRC Bulletin 93-03,

"Resolution of Issues

Related to Reactor

Vessel

Water Level Instrumentation

in BWR's".

The licensee

planned to.install the modification either during the next forced

outage of sufficient duration or during their next planned

refueling outage in April 1994.

Back round

The licensee initiated this modification to address

a generic

concern for dissolved

gases

accumulating in the reference

legs of

the reactor vessel

water level instrumentation

in boiling water

reactors

(BWR).

A high concentration of dissolved

gases

in the

reference

legs

has the potential to cause reactor vessel

water

level deviations

known as "notching".

A generic modification had

been developed

by the Boiling Water Reactor

Owner's

Group

(BWROG)

to continuously backfill the reference

legs with water containing

a low dissolved

gas concentration

in order to reduce the

concentration of dissolved

gases.

-11-

Potential

problems with this generic modification were described

in NRC Information Notice 93-89, "Potential

Problems with

BWR

Level Instrumentation Backfill Modifications".

The information

notice described

the potential effects of the inadvertent

closure

of a existing manual

root valve in the instrument line and the

severe reactor transient

which would result.

At WNP-2, the modification also introduced

a potential

pressure

source

from the Control

Rod Drive (CRD) system,

which provided

a

small continuous backfill.flow into each reference

leg for the

level instrumentation.

Inadvertent isolation of a reference

leg

from the reactor vessel

would result in the reference

leg being

pressurized

by the

CRD pump, thereby causing the instrumentation

connected to the reference

leg to indicate erroneous

plant

conditions.

Each reference

leg supplied other instruments

in

addition to the reactor vessel

water level instrumentation.

For

the worst case,

one

common reference

leg supplied the pressure

switches

associated

with automatic opening of 18 safety relief

valves

(SRVs).

Consequently,

the inadvertent pressurization

of

the one reference

leg that controls the actuation of the

18 SRVs

would result in the lifting of all

18 SRVs

and

a blowdown of the

reactor coolant inventory.

At WNP-2 all of the

18 SRVs can

be self-actuated

(spring lift) or

power-actuated

(pneumatic).

The

SRVs self-actuate

to lift as

ASME

Code safety valves.

In addition, the

SRVs are actuated

automatically to control

steam pressure

during

a large load

rejection.

Additionally, the Automatic Depressurization

System

(ADS) utilized seven of the

SRVs as part of the

ECCS system to

blowdown the reactor coolant system in the event of a small break

LOCA, to allow the function of low pressure

injection.

However,

the inadvertent pressurization

of one instrumentation

reference

leg would only actuate

one channel of the sub-logic for the

ADS,

but would not cause

an actuation of the

ADS.

Observations

The inspector

found that the licensee

had evaluated

Information Notice 93-89

and the consequences

of inadvertent

instrumentation

line root valve closure

as part of their safety evaluation for the

modification.

For the worst case

instrument line, the licensee

had determined that the inadvertent closure of the .manual

isolation valve with the backfill system in operation would

increase

pressure

in the instrument line up to the

CRD system

pressure

of 1450 psi, which exceeded

the normal reactor

pressure

of 1050 psi.

The instrument line pressurization

would result in

the simultaneous

false signals of low reactor vessel

water level

and high reactor pressure.

The false high reactor pressure

signal

would actuate

the pressure

switches for all of the

18 safety

relief valves

(SRV) because

the pressure

sensed

was from one

common instrument line.

Since the normal

CRD pressure

exceeded

12

the setpoint for the

SRV relief function, all

18

SRVs would open

and blowdown of the reactor coolant system into the suppression

pool would occur.

The licensee

indicated that this blowdown would

not be bounded

by the

FSAR analysis,

which addressed

only the

inadvertent

opening, of one

SRV.

Another consequence

of the inadvertent pressurization

of an

instrument line was that

one 'division of the residual

heat

removal

and low pressure

core spray

(RHR/LPCS)

systems

would be inhibited

due to the false high reactor pressure

signal.

Despite actual

depressurization

of the reactor coolant system resulting from the

SRV blowdown, the low pressure

permissive interlocks for the

RHR/LPCS injection valves would prevent the valves from opening

due to the false high reactor pressure

signal.

However, the other

division of RHR/LPCS low pressure

injection would be available,

unless

a single failure was

assumed.

The most critical single

failure that the licensee

assumed

was the failure of the low

pressure

injecti'on line interlock for the opposite division.

In

that case,

the licensee

concluded that the operators

would not

have low pressure

injection available

and core

damage

would most

likely result,

except

as mitigated

by the

Emergency Operating

Procedure

(EOP) actions for beyond-design-basis

accidents

using

nonsafety-related

systems for core flooding.

The inspector

discussed

the vulnerability of the licensee's

design

in comparison with the other designs

referenced

in Information Notice 93-89.

The inspector

found that the operators

at

WNP-2 did

not have

a keylock switch to bypass

the low pressure

injection

interlock permissive

as described

in the information notice

as

a

mitigating feature at another utility.

The WNP-2 backfill

injection point was

on the instrument rack side of the manual

isolation valve.

Other utilities referenced

in the information

notice with this design

had revised their original design to

inject on the reactor side of the manual isolation valve.

The inspector

noted that the licensee's

original design

recognized

the potential for the reactor coolant

blowdown scenario,

but the

licensee

had concluded that they had implemented

adequate

administrative controls to prevent the inadvertent closure of the

instrument root valves.

The administrative controls consisted of

a chain

and lock for the valve handwheel,

which was procedurally

controlled.

Because of the severe,

unanalyzed

event which could

occur at WNP-2 following the inadvertent closure of one

instrumentation line root valve, the inspector

was concerned

that

the licensee's

measures

to preclude inadvertent closure did not

appear to be appropriate.

Later, during the inspection, the

licensee

decided that more positive control of the valve was

warranted.

The licensee initiated

a revision to their design to

weld

a device

on the

open root valve to preclude valve operation.

The licensee

has committed to complete this design modification

for the one root valve which affects all eighteen

SRV's.

- 13-

The inspector

also noted

an additional potential for an event

initiator beyond the potential for inadvertent closure of the

instrumentation

root valve discussed

in Information Notice 93-89.

The inspector

noted that the instrumentation

tubing from the

instrument rack to the root valve was exposed

to potential

damage

and inadvertent

crimping.

At the time of inspection,

the tubing

was in an area

where scaffolding

had

been erected for an upcoming

unrelated modification.

The tubing had

a 1/2-inch outer diameter

and

a wall thickness of 1/16-inch.

Therefore,

the inspector

concluded that it was susceptable

to being crimped or crushed.

In

addition, the tubing contained

an expansion

loop which appeared

to

be especially vulnerable to damage.

Additionally, the inspectors

noted that there

was

a potential for

a foreign object to block the small

passages

in the line.

Compo-

nents,

such

as the excess

flow check valves

and flow limiting

orifices, contained restricted

passages

which could become

blocked

by foreign objects

from normal maintenance

tasks

on the instrument

racks.

The inspector

recognized

the fact that maintenance

work is

performed under cleanliness

controls,

but was concerned that these

controls

may not be completely effective to preclude the

occurrence.

The inspector

also noted that there could

be other

methods for line blockage,

which had not been

addressed.

Discussions

with the licensee

indicated that the blocking of the

instrumentation line, the opening of all eighteen

valves to the

suppression

pool,

and the subsequent

reactor transient

were not

bounded

by accidents

described

in the

FSAR.

10 CFR 50.59 Evaluation

The inspector

reviewed the

10 CFR 50.59 evaluation

performed

by

the licensee for the backfill modification and discussed

the basis

for the licensee

evaluation with cognizant licensee

personnel.

The licensee

had concluded that the modification did not involve

an unreviewed safety question.

The licensee

considered that the

circumstances

necessary

to block the instrument line either

through valve closure or any other mechanism

were not credible

occurrences.

The licensee

considered that the potential

accident

resulting from the closure of the root valve with the backfill

system in operation

was less likely than the events

analyzed in

the

FSAR since closure of the root valve would require,

what the

licensee

considered

to be,

two active failures (or operator

errors).

The licensee

stated

the first failure (or error) would

be the issuance

of the key by the shift supervisor

and the second

failure would be the use of the key by an operator to unlock and

close the valve.

The licensee

stated that the modification met

the single failure design criteria since

no single failure would

result in closure of the root valve.

Therefore,

the licensee

considered that they had met the single failure criteria and

had

established

adequate

preventative

measures

to assure that

a new

accident scenario

would not be introduced

by the modification.

-14-

The licensee identified that their

10 CFR 50.59 evaluation

used

two screening criteria for addressing

the question of whether

a

new accident

cou')d

be created

by a modification.

The first

criteria addressed

whether

a new accident

could

be created.

The

second criteria addressed

whether that

new accident

was credible.

The licensee

used the industry guidance

contained

in Nuclear

Management

and Resources

Council,

NSAC 125, "Guidelines for

10 CFR 50.59 Safety Evaluations," in'onducting their 10 CFR 50.59

evaluation.

The guidance

contained

an example which stated that

meeting the single failure criteria was sufficient.

That is, if

multiple safety system failures were required to initiate

a new

accident,

then the

new accident

would not be considered

credible.

The guidance established

that meeting the single failure design

criteria assured

that the probability of occurrence of subsequent

accidents

due to the failure of the safety

systems

to perform

their safety function would be equivalent to that of the accidents

originally analyzed in the

FSAR.

The licensee's

10 CFR 50.59 evaluation for the backfill

modification considered that multiple failures of administrative

controls would be required to initiate the

new accident.

The

licensee

also considered

that the redundant administrative

controls satisfied the single failure criteria for the system

design,

in that multiple administrative failures would be required

to initiate the accident scenario.

As

a result,

the licensee

concluded that the modification did not introduce

an accident of a

new type because their design satisfied their interpretation of

single failure criteria.

The inspector did not agree with the

licensee's

interpretation that the breaching of two administrative

control systems

would constitute

two independent

single failures.

The inspector considered that the closure of a single valve

constituted

a single failure, regardless

of how many

administrative control boundaries

were established.

Conclusions

The inspector

concluded that the engineering

and technical

support

groups

had

been actively involved in the development of the

modification for the backfill system.

For example,

the licensee

had participated

in the

BWROG testing in the development of the

generic modification,

and

had conducted

extensive

mockup testing

and preoperational

system testing

had

been

conducted to verify and

optimize the system performance prior to installation.

In

addition, the inspector

found that the licensee

had coordinated

inputs from Operations,

Maintenance,

Engineering

and industry in

the expeditious

development

and installation of the modification.

However, the inspector identified unresolved

concerns

in the

following areas:

~

The adequacy of the proposed backfill modification from the

standpoint of the credibility of initiating an unanalyzed

event through the blockage of a single instrumentation line

from any line blocking mechanism.

~

The adequacy of the licensee's

10 CFR 50.59 review and

safety analysis

determining whether the modification

involved an unreviewed safety question.

The licensee

acknowledged

the inspector's

concerns.

These

concerns wil'i be considered

an unresolved

item pending further

NRC

review.

(Unresolved

item 50-397/94-02-01)

Excess

Flow Check Valves

The inspector identified

a separate

issue regarding

containment

integrity as

a result of the review of the

BWR backfill

modification.

The inspector

had reviewed the design of the excess

flow check valves installed in the instrument lines involved in

the backfill modification for the reactor vessel

water level

instrumentation.

The inspector

found that the excess

flow check

valves contained

an integral

manual

bypass

valve which was

normally closed.

However,

these

manual

bypass

valves

had not been

included in the list of manual

containment isolation valves that

were required to be locked closed or verified shut every 31 days

in accordance

with the Technical .Specification requirements.

The function of the manual

bypass

valve was to temporarily

equalize

pressure

across

the excess

flow check valve after

actuation of the excess

flow check valve.

This allowed the check

valve return spring to restore the check valve to an open

position.

The inspector found that the manual

bypass

valve was

not uniquely identified on the plant drawings.

In addition, there

was

no position indication for the manual

bypass valve, either

locally or remotely in the. control room..'The inspector

was

concerned that, if the valve was left open, it would bypass

the

excess

flow check valve which was credited in the

FSAR as

an

automatic containment isolation valve in accordance

with the

guidance of Regulatory Guide l.ll, "Instrument Lines Penetrating

Primary Reactor Containment."

The licensee

indicated that they had

an informal practice of

removing the valve handle after closing the valve and storing the

handle in the control

room to preclude unauthorized

manipulation.

However, the inspector noted that several

manual

bypass

valve

handles

were installed,

which indicated that this informal

practice

was not always carried out.

In response

to the inspector's

concern,

the licensee initiated

PER

240-032.

The licensee

performed

a surveillance of all accessible

-16--

excess

flow check valves

and found that they were all correctly

positioned.

Based

on the results of their surveillance,

the

licensee

concluded that all the manual

bypass

valves

were closed.

In addition, the licensee

added the manual

bypass

valves to

Surveillance

Procedure

PPH 7.4.6.1. 1 pending the resolution of the

PER.

The licensee

stated that they did not consider the Technical

Specification surveillance

requirement to be applicable to the

manual

bypass

valves.

Although they noted that the excess

check

valves were identified in Technical Specification Table 3.6.3-1

as

containment isolation valves,

they stated that neither the excess

flow check valves,

nor the integral

manual

bypass

valves were

required to close in an accident.

The licensee

stated that they

based their position

on the

FSAR Chapter

15 analysis of the

blowdown and dose

consequences

which did not take credit for the

check valve functioning in the event of an instrument line break

outside of containment.

Nevertheless,

the inspector

concluded that the excess

flow check

valves were required to be closed in an accident.

The inspector

based this position

on the following Technical Specification

requirements

for operable

excess

flow check valves

and the

guidance of Regulatory

Guide

1. 11.

Technical Specification 3.6.3 required that the reactor

instrumentation line excess

flow check valves,

shown in

Table 3.6.3-1 to "...be

OPERABLE during

OPERATIONAL

CONDITIONS 1,

2 and 3."

Regulatory Guide 1.11 provided guidance that each

excess

flow check valve should function as

an automatic isolation

valve in order to satisfy General

Design Criteria 55 and

56

(for containment integrity).

Regulatory

Guide 1. 11 stated that "...there should

be

a high

probability that the valve...will close if the instrument

line is ruptured downstream."

Regulatory

Guide l. 11 provided guidance that each instrument

line contain

a flow-restricting orifice appropriately sized

to independently limit the consequences

of an instrument

line failure outside of containment.

The inspector found

that the

FSAR Chapter

15 analysis

supported

the appropriate

sizing of the orifice; however,

the

FSAR analysis did not

obviate the need for the excess

flow check valves to perform

the safety function to automatically close

as isolation

valves.

FSAR Paragraph

6.2.4.3.2.4

stated,

in part,

"The Excess

Flow

Check

(EFC) valves

each

have

an integral

manual

bypass

valve

17-

which may be used to reset

an actuated

disc.

In order to

minimize a possible potential

impact upon the integrity and

functional performance of the secondary

containment

and its

associated filtration systems

should

an instrument line

failure occur, the bypass

valves

are periodically verified

to be closed."

Conclusion

Technical Specification 4.6.1. l.b required that all non-automatic

containment isolation valves that are required to be closed during

an accident

be checked monthly to demonstrate

primary containment

integrity.

Licensee

procedure

PPH 7.4.6. 1. 1, "Primary Containment

Integrity Verification," implemented

the surveillance

requirement

of TS 4.6.). l.b.

The inspector

found that the manual

bypass

valves for 115 excess

flow check valves identified in Table 3.6.3-

1 were not included in the Surveillance

Procedure

PPH 7.4.6.1. 1.

The failure to verify that the manual

bypass

valves for the

115

excess

flow check valves specified in Technical Specification

Table 3.6.3-1

were closed or locked in their closed position is

a

violation of Technical Specification 4.6.1. 1.b. (Violation 50-

397/94-02-02)

4.1.2.4

Incorrect Orifice Size

The inspector identified .another

problem regarding

improper

instrument line orifice sizes

as

a result of the review of the BMR,

backfill modification.

The inspector

found that the Haster

Equipment List (HEL) identified that 0.375-inch diameter orifices

were installed in the instrument lines for the water level

instrumentation.

However,

FSAR Chapter 15.6.2,

"Instrument Line

Break Analysis," indicated that the blowdown analysis for a

rupture of an instrument line was based

on )/4-inch diameter

orifices.

The licensee

subsequently

determined that the larger

orifices had been .installed during original construction

and

potentially affected all

115 instrument lines.

The licensee identified that

an orifice was installed in each

instrument line per Regulatory

Guide 1. 11 to limit releases

in the

event of a break of the instrument line to 10 CFR Part 100 limits.

Regulatory

Guide 1.11 stated that the combination of an orifice

and excess

flow check valve was

an acceptable

alternative

design

for two automatic isolation valves for the containment isolation.

In addition, the licensee

indicated that their

FSAR safety

analysis calculations for offsite releases

had

been

based

on the

1/4-inch orifice sizes.

The licensee initiated

a problem evaluation request

(PER)

on

January

27,

1994, to resolve the issue.

Their initial analysis

indicated that the larger size orifice would be acceptable

and not

significantly change

the

FSAR Chapter

15.6.2 analysis.

The

-18-

licensee

also stated that they considered that they would be able

to justify the adequacy of the larger orifices, recognizing the

fourfold increase

in the blowdown into the secondary

containment

and the dose

consequences.

The inspector considered that the initial licensee

actions

were

adequate.

However, this item is considered

an unresolved

item

pending review of the licensee's

evaluation of the radiological

consequence,

and the root cause of the discrepancy

between

the

as

.

built orifice sizes

and the

FSAR description.

(Unresolved

item 50-397/94-02-03)

1

4.1.3 Conclusions

4.2

The inspector concluded that engineering

appeared

to be actively

involved in ongoing modifications.

For example,

they were actively

involved in the identification and resolution of a longstanding

technical

issue involving leaking containment

supply

and exhaust

isolation valves.

The inspector also observed that engineering

had

been

actively involved in the development of the reactor vessel backfill

modification.

Their activities included involvement with the

BWROG in

the development of the modification,

as well as close coordination with

operations

and maintenance.

The inspector

concluded that the licensee

performance

in the

impl.ementation of the reactor vessel backfill modification could have

been

improved.

Specifically, the inspector identified unresolved

items

regarding,

(1) the credibility of initiating an unanalyzed

event through

the blockage of a single instrumentation line; (2) the adequacy of the

licensee's

10 CFR 50.59 review and safety analysis;

and

(3) improper

instrument line orifice sizes.

The inspector also identified a

violation involving the licensee's

failure to periodically verify that

the manual

bypass

valves for the

115 excess

flow check valves were

closed

o) locked in their closed position.

Completed Nodifications

4.2.1

Sample

and Criteria

The inspector performed

a limited review of completed modifications.

In

addition,

NRC Inspection

Report 50-397/93-25,

issued

August 13,

1993,

examined six design

changes for conformance to regulatory criteria.

That inspection

found that the design

changes

generally

met the

regulatory criteria.

However, the inspection

also identified one

violation for failure to update preventative

maintenance

records

pursuant to the modification.

During this inspection,

the inspector

reviewed several

modifications

including Plant Modification Request

(PHR) 91-0309-0,

"Diesel Generator

Heat Exchanger Service

Water

Flow Balance."

The objective of the review

was to assess

whether the modification package

was well-organized,

the

-19-

4.3

modification was clearly described,

the design calculations

were

correct, the

10 CFR 50.59 evaluations

were adequate,

and the post-

modification test requirements

and acceptance

criteria were accurately

specified.

4.2.2 Findings

The inspector found that the modification met the regulatory

requirements.

However, the inspector

noted

one minor discrepancy

wherein the modification description

was not clear.

Specifically, the

modification description stated that, "It is the intent of this

modification to distribute at least

45K of the total service water flow

to the two heat exchangers

in each loop to any one heat exchanger....

Additionally, the ability to achieve

a combined flow rate of 1650

gpm

for both heat exchangers

in each loop must

be confirmed."

The inspector

noted that 45 percent of 1650

gpm is 742.5

gpm, which was less than the

825

gpm described

in the reason for the modification.

The licensee

agreed that the reference

to 825

gpm in the modification package

was

misleading.

The inspector's

observation

did not constitute

a safety

concern,

and was provided to the licensee

as

an observation.

4;2.3 Conclusions

Based

on the results of Inspection Report 50-397/93-25

and this

inspection,

the completed modifications generally

appear to meet

regulatory requirements.

Temporary

and Minor Modifications

The inspector reviewed the licensee's

overall program for control of

Temporary Hodifications

(THODs).

The purpose of the review was to

determine

how well the licensee

was managing the

number of THODs and the

level of involvement by operations

and engineering

personnel

in the

THOD

process.

4.3.1

Sample

and Criteria

The inspector reviewed the licensee's list of active

THODs and selected

two safety-related

modifications for review.

This review included

discussions

with the system engineer

and operators

concerning the

modification,

and

a field verification of the modification installation.

The purpose of the review was to determine if: (1) the

THOD was

developed,

reviewed,

and implemented

per plant procedure

manual

(PPH)

1.3.9,

"Temporary Hodification Control," (2)

a proper

10 CFR 50.59

evaluation

was conducted,

(3) plans to restore

the

THOD or install

a

permanent

design

change existed,

and (4) all necessary

technical

and

regulatory requirements

were addressed

in the

THOD.

4.3.2 Findings

4.3.2. 1

Overall

Program

Review

The inspector

noted that the number of active

THODs was reduced

from 34 in April 1993 to 15 with a goal of 10 after the next

refueling outage.

One shift manager

was assigned

to ensure that

operations

personnel

played

an active role in the

THOD process.

Participation in the process

was evident

by the knowledge the

operators

had concerning .the status of the active

THODs,

and also

by routine audits of the

THOD log.

,Several of these audits

identified administrative errors in some of the

THODs,

and the

shift managers

were holding the system engineers

accountable

to

correct the errors.

Although this type of management

oversight

was not evident earlier in 1993

(see

NRC Inspection

Report 50-

397/93-24),

the inspector

concluded that the licensee

had improved

their oversight of THODs.

4.3.2.2

Hain Steam Isolation Valve (HSIV) Modification

The inspector

reviewed Temporary Modification Request

(THR) 93-

004.

This

TMOD installed resistance

temperature

detectors

(RTDs)

on the main steam isolation valve (HSIV) limit switches in the

steam tunnel to establish

an accurate

temperature profile for the

limit switches.

The limit switches

were moved in 1990

as part of

a design

change

so that they were further from the steam lines.

The

TMOD was installed to quantify the actual

temperature profile

so that the equipment qualification (Eg) life of the limit

switches could be validated.

The limit switches

had

a calculated

Eg life of 2.7 years,

and were replaced

every two years.

"

The inspector

concluded that the

THOD was properly processed

and

installed per 'the licensee's

procedures.

Additionally, the

10 CFR 50.59 safety evaluation

was thorough.

For example,

the effect of

the additional weight of the

RTDs on the seismic design

requirements

was included in the evaluation.

Overall, the

inspector concluded that the installation of the

THOD was

a good

initiative by engineering.

4.3.2.3

Disabled Control

Room Annunciator

t

The inspector reviewed

THDD 92-012,

which was installed in 1989.

This

THOD disabled

a continuous

annunciator

alarm input caused

by

the abnormal position of the switch in the fire remote transfer

panel

(FRTP) for Fan WA-53B, the recirculation fan for the

Division 2 switchgear

room.

The switch was purposely kept in the

abnormal

emergency position to ensure that the control for this

fan was maintained at the

FRTP.

This was necessary

as

a temporary

remedial

action

due to

a licensee-discovered

condition where

a

degraded

voltage condition would prevent starting the fan from the

control

room.

The fan operation

would be satisfactory if the fan

-21-

were started

from the

FRTP.

This problem with the degraded

voltage condition was documented

in LER 89-013,

Plant Engineering

Request

(PER) 2-89-0323,

and Nonconformance

Report 289-0322.

By

disabling this particular annunciator,,an

alarm would be received

if any of the other remote transfer switches

were placed in the

emergency position.

The inspector

observed that the appropriate

plant procedure

manual

(PPH)

had been

changed to allow control of

the fan from the

FRTP.

Additionally, the inspector

noted that the

10 CFR 50.59 screening

process

at the time of the change (i.e.,

1989) did not require

an

evaluation or justification of the abnormal condition since the

normal location of fan control

was not described

in the Final

Safety Analysis Report.

However, the inspector

noted that the

licensee

had recently improved their 10 CFR 50.59 process

due to

weaknesses

identified in NRC Inspection

Report 50-397/93-36.

The

licensee's

new procedure for 10 CFR 50.59 evaluations

would have

required. an evaluation of the condition.

The inspector further

concluded that,

even though

an evaluation

was not performed,

normal operation of the fan from the

FRTP did not adversely

impact

overall plant safety.

The inspector

concluded that

a permanent solution for the problem

had not been aggressively

pursued

by the licensee.

Even though

the licensee

stated in LER 89-013 that the operation of the fan

from the

FRTP was

a "temporary solution", the licensee

allowed the

abnormal situation to exist for almost five years.

The inspector

noted that

a plant modification request

(PHR) was initiated to

correct the problem by installing

a voltage regulator in the

control

room starting circuit; but the

PHR was continually

deferred

due to higher priorities.

The inspector also noted that

the licensee's

current efforts to identify and reduce the number

of old THODS also identified this particular delay in implementing

a correction to the situation.

As

a result,

PHR 92-083

was

approved

and scheduled for refueling, outage

R-9.

Inadvertent

Design

Changes

The inspector

reviewed completed valve lineup sheets

and the

Component Status

Change Order

(CSCO) log to determine if any

inadvertent

design

changes

had

been introduced

by the changes

to

the valve lineups.

The inspector identified one inadvertent

design

change

and

a valve lineup discrepancy.

Post Accident

Sam le

S stem

PASS

Demineralized

Mater

DW

valves

The inspector noted that valves

DW-757 and DW-758, which are

DM

supply isolation valves for the residual

heat

removal

(RHR)

PASS

sample flush lines,

had

been cautioned-tagged

shut since

1987.

The valves were originally shut in 1987 due to leakage

past

two

isolation valves

and

a check valve which caused

contamination of

-22-

the

DW system

from the

RHR system.

One of the isolation va')ves

and the check valve were repaired;

however,

DW-757 and

DW-758

remained

shut

as

a precaution to preclude further

DW

contamination.

The primary isolation valves,

PSR-Y-003A and

PSR-

V003B, were not repaired.

There

was

an

open work order for

these valves,

but it continued to be deferred.

The inspector

observed

a chem'istry technician simulate taking

a

PASS sample

from the

RHR system

and noted that the procedure

being

used could not be completed

as written since the sample lines

could not be remotely flushed per the procedure's

requirements.

Entry into high radiation

areas

would have

been required to

manually open the isolated valves.

The inspector

concluded that

keeping the

DW valves shut for seven years

was

an inadvertent

design

change in that the ability to remotely flush the sample

lines was removed.

Although

PER 293-317

had

been written, it only

documented

the problem with the system leakage.

The licensee

had

not evaluated

the effect of not being able to flush the sample

lines

on general

area radiation levels if a sample

was required

during

an accident.

The inspector concluded that the safety significance of the

inability to remotely flush the

PASS sample lines after

an

accident

sample

was minimal because

operability of the

PASS system

was not affected

and there

was

no requirement to perform the

flush.

However, the inspector

noted that the flush was

a prudent

measure to reduce general

area radiation levels.

PASS Valve Lineu

Discre

anc

During a review of the

CSCO log in the control room, the inspector

noted that manual isolation valves

RHR-746 and

RHR-747 were listed

as shut.

The valves were

on

PASS sample lines from the

RHR

system.

The normal position of the valves

was open to allow

obtaining

a remote

PASS sample of the

RHR system using other

solenoid-operated

valves.

The date of the

CSCO sheet

was Hay 1,

1993.

Further

review identified another record,

the master

system

valve lineup, which indicated that the valves were opened

on

June

10,

1993.

The licensee

conducted

a field .verification and

determined that the valves were opened

as

shown

on the master

system valve lineup.

The licensee

then corrected

the

CSCO entry.

The inspector

noted

a procedure

weakness,

in that the

administrative

procedures

for controlling the

CSCO log did not

provide any instructions to review the

CSCO for necessary

updates

after performing the master

system valve lineups.

-23-

Corrective Actions

The licensee

conducted

an audit of the

CSCO log and the master

valve lineup data sheets

and identified several

other

discrepancies

between the valve lineups

and the

CSCO log.

None of

these

errors were safety significant.

In response

to this

concern,

the Operations

Hanager instituted

a new administrative

requirement to audit the

CSCO logs every 28 days.

In addition,

the license initiated

a change to

PPH 3.1. 1, "Haster Valve

Lineup," to require shift managers

to review the

CSCO when

a

master lineup was completed.

The inspector concluded that the

licensee's

actions

were appropriate.

4.3.3 Conclusions

The inspector

concluded that the licensee

had initiated programs

which

significantly improved their oversight

and management

of the

THOD

program.

Additionally, program oversight

appeared

to be effective, in

that the age

and number of temporary modifications were being

significantly reduced.

Although the inspection identified one minor problem regarding

a

longstanding

temporary modification involving an abnormal position of

the switch on the fire remote transfer

panel for the recirculation fan

for the Division 2 switchgear, this problem had

been previously

identified by the licensee's

program

and corrective action

had already

been scheduled for the next outage.

Two minor problems were identified in the area of temporary

modifications.

One problem involved an inadvertent

design

change to the

PASS system

caused

by closing normally-open,

manually-operated,

demineralized

water valves.

As

a result,

the ability to remotely flush

portions of the

PASS to reduce

area radiation levels

was removed.

A

second

problem involved

a weakness

in the administrative

procedures

for

control,ling valve lineup exceptions.

The licensee

took appropriate

corrective action for these

problems.

No violations or deviations of NRC requirements

were identified.

5.0

5.1

Engineering

Involvement in'lant Problems

Nonconformance

Review

5.1.1

Sample

and Criteria

The inspector reviewed the Quality Assurance

(QA) procedures

addressing

the identification and processing of plant problems to verify

conformance with regulatory requirements.

The inspector selected

15

Nonconformance

Reports

(NCRs) out of a total of 64 issued in 1993.

These

15

NCRs were reviewed for evidence of engineering

involvement with

the resolution.

-24-

5.1.2 Findings

NCR Review

The inspector found that

11 of the

15

NCRs required,

and received,

engineering

support in resolving the technical

issues

affecting the

plant.

Engineering

support

was evident in the form of design

changes,

design calculations,

evaluations of proper set points,

performance of

probabilistic risk analysis

(PRA),

and root cause analysis.

The

remaining four NCRs required

no engineering

input.

Lack of Overview of PERs

The inspector

observed that Plant Procedures

Hanual

(PPH) 1.3. 12,

"Problem Evaluation

Request

(PER)," described

the method for initiation

of a

PER to report potential

or actual

conditions adverse

to quality.

PPH 1.3. 12, Section 6.0, required that

an individual discovering

a

condition adverse

to quality document the condition by initiating a

PER.

However, not all potential plant problems

were required to be logged in.

Only those

problems

determined

by the supervisor

as being valid were

logged in and assigned

a

PER number.

Problems judged not to warrant

a

PER were returned to the originator with the reason

described

on the

form.

5.2

The inspector

concluded that

PPH 1.3. 12 did not provide strong

provisions for overview of non-valid

PERs.

The inspector

was concerned

that in the event of an error in judgement

on the part of the supervisor

potential plant problems

which might represent

actual

conditions

adverse

to quality would not receive

any oversight.

The licensee's

process

did

not provide for any additional

overview beyond the supervisor's

screening.

The inspector discussed

his concerns with the licensee.

The licensee

committed to revise

PPH 1.3. 12 to require non-validated

PERs to be

filed, and also to perform periodic quality assurance

audits of the

files.

The licensee's

actions will be reviewed in a future inspection.

{Followup It'em 50-397/94-02-04)

5.1.3 Conclusi.ons

The inspector

concluded that the sampled

nonconformances

indicated that

engineering

involvement was evident in the identification and resolution

of technical

issues

affecting the plant.

Engineering

Involvement in the Reactor

Pressure

Vessel

(RPV)

Nozzle/Safe-End

Stress

Improvement

Process

5.2.1 Sample

and Criteria

The inspector

assessed

engineering

involvement through

an examination of

the engineering

controls over

a planned,

complex,

maintenance activity

-25-

which involved the reduction of reactor pressure

vessel

{RPV) stresses.

The inspector

examined the selection of the contractor,

the review of

contractor procedures,

and the adequacy of contractor quality control.

The purpose of this review was to evaluate

the adequacy of engineering

involvement

and to ensure

compliance with regulatory requirements

and

industry codes

and standards.

5.2.2 Findings

In response

to

NRC Generic Letter 88-01,

"NRC Position

on

IGSCC in

BMR

Austenitic Stainless

Steel Piping," dated January

25,

1988, the licensee

was planning to perform stress

improvement

on 44 weld joints of the

RPV

nozzles

and safe-ends.

The stress

improvement technique

planned

was the

use of the Mechanical

Stress

Improvement

Process

(HSIP).

NSIP was

considered

by the

NRC technical staff to be

a qualified process

for

~

providing resistance

to intergranular

stress

corrosion cracking

{IGSCC)

in

BWR austenitic stainless

steel piping.

The stress

improvement

was

scheduled

to be completed

in 11 days during the next refueling outage

in

April 1994.

The inspector reviewed the procurement

documents that qualified the

contractor,

AEA O'Donnell, Inc., to be placed

on the licensee's

Evaluated Supplier List (ESL).

The audit of the contractor

was

performed

by the Nuclear Procurement

Issues

Committee

(NUPIC),

an

external

organization

whose

members

represent

various nuclear utilities

and licensees.

The inspector

found that Procurement

Engineering's

evaluation of the

NUPIC audit appropriately

addressed

the licensee's

requirements

for the scope of work to be provided.

The inspector also

found that the contractor's

gA program included controls of their

subcontractors.

The inspector

reviewed Contract

Number

C30831,

dated

December

8,

1993,

for AEA O'Donnell, Inc.

The inspector verified that the contract

included

a provision that the supplier have

a documented guality

Assurance

(gA) program that:

(1) complied with the requirements of

10 CFR 50, Appendix B, and (2) extended

appropriate

gA requirements

to

sub-tier suppliers.

The inspector also confirmed that the contract

included supplier acknowledgement

for reportability pursuant to 10 CFR Part 21, "Reporting of Defects

and Noncompliance."

Contract

C30831,

Appendix A, "Statement of Mork," required the

contractor to provide the following to the Supply System .by January

14,

1994:

(1) procedures

that would be used for the stress

improvement

process,

and (2) information about

any special

equipment that would be

brought

on site.

The inspector

was informed by the licensee that both

these

requirements

were met by the required date.

Licensee responsibilities for the MSIP program were

shown in

Attachment

5 of Contract

C30831.

Specific responsibilities

included

approval of the

AEA O'Donnell, Inc., engineering

procedures,

training

program, field service procedures,

and nonconformance

reports.

Review

-26-

and approval of the contractor quality control

(gC) inspector's

qualifications

was specified in the contract

as

a licensee

responsibility.

During the inspection,

the licensee

was in process

of

revising the contractor's

HSIP traveler to include the licensee's

engineering

review and verification of process

acceptance.

5.2.3 Conclusions

5.3

The inspector

concluded that engineering

was actively involved in the

RPV nozzle

and safe-end

stress

improvement process

planned for the

upcoming outage.

This was evident

by the amount of engineering

oversight

and quality controls over the contractor's

mechanical

stress

improvement process.

Materhammer

Incidents in the Standby Service Mater System

(SSMS)

5.3. 1 Sample

and Criteria

The inspector reviewed engineering

involvement in waterhammer

incidents

in the Standby Service Water System

(SSWS).

The inspector reviewed the

completeness

and accuracy of the problem evaluation reports

(PERs)

including root cause

evaluations

and interim dispositions.

The

inspector also examined Engineering's

support to Systems

Engineering for

this problem.

5.3.2 Findings

The

SSWS

had experienced

waterhammer

problems for several

years.

The

problem occurred following pump starts

due to the fact that the system

piping drained

and emptied

when the system

was not in service.

The

licensee's

operational

strategy for avoiding these

waterhammer

events

was to automatically fill the system through

a time-sequenced,

controlled opening of Hotor-Operated

Valves

(HOV) SW-V-2A and

SW-V-2B

just downstream of SSWS

pumps

SW-P-1A and SW-P-18.

The valve opening

scenario

consisted of a 12-second

stroke time from full closure,

which

resulted in the valve opening approximately

20 percent;

followed by

a

50-second

hold period in the throttled position.

This sequence

allowed

flow to be gradually established

in the

SSWS,

and filled the system at

a

substantially

lower flow than full flow.

After the 50-second

hold

period, the valve resumed

opening to full-open position.

During a

previous inspection in February

1993, the inspectors

had examined the

waterhammer

problem,

discussed

the licensee's

operating strategy to

avoid waterhammer,

and witnessed

a test which demonstrated

the

satisfactory

system start without waterhammer.

The inspector discussed

the additional

waterhammers

that

had occurred

since the last team inspection

and examined the circumstances

surrounding the

new occurrences.

- 27

Valve 'Overstroke

Caused

Waterhammer

On November

15,

1993,

Loop

B of the

SSWS experienced

a waterhammer

event.

Problem Evaluation Request

(PER)

293-1319

was written to

investigate this event.

The licensee attributed the waterhammer

event

to the fact that butterfly valve SW-V-2B'ad overstroked its closed

position by 13 percent.

This condition was discovered after the valve

was

opened

and inspected.

At its closed position, the valve disk had

passed its central

stop position (i.e., the middle of the seating

surface).

This condition was possible with the particular butterfly

valves in use

because

of their large seating

surface.

As

a result of

the overstroked position, the licensee

determined that the valve had

opened only 3 to 5 percent

instead of the intended

20 percent during the

fitst

12 seconds of valve opening,

Consequently,

during the subsequent

50-second

hold period,

very little to no flow was provided to fill the

SSWS.

The licensee

confirmed this theory with plant computer data,

which indicated minimal to no flow had

been achieved.

During the

subsequent

stoke of the valve to the full-open position, flow entered

the almost empty

SSWS at substantial

flow rates

and caused

a

waterhammer.

Inade uate Guidance in Settin

Valve to Its Full

Closed Position

PER 293-1319 stated that the root cause for valve SW-V-2B overtravel

was

inadequate

guidance in the Motor-Operated

Valve

(MOV) Master

Data Sheet.

The Master

Data Sheet

contained

applicable information on the

MOV such

as switch setting

and stroke time requirements.

It did not contain

information which required the closed position to be checked for angle.

The overtravel condition was established

when

a closed limit switch

adjustment

was

made

on May 14,

1993, during

a baseline

MOV test.

The

licensee's

test procedure

required the Master Data Sheets

to be used

along with the maintenance

work request for setting

up the valve

parameters.

The licensee

stated that during the

MOV baseline test,

the

technicians

followed the standard practice of adjusting the closed limit

switch until an increase

in the torque required to close the valve was

detected.

This practice

had

been successful

previously

on butterfly

valves with small seating

areas,

but was apparently not appropriate

for

valve SW-V-2B, which had

a large seating

area

and needed to open to a

precise throttle position.

The wide seating

surface

introduced

a

substantial

error in the opening

angle to initiate flow.

The licensee

stated that they planned corrective action .to revise the

Master Data Sheet to specify that valve SW-V-2B was fully closed

when

the stem keyway was directly in line with the

SW pipe centerline,

thus

eliminating the angular error.

The inspector considered

the licensee's

action appropriate.

A

arent Differences in Valve 0 enin

Times

In examining the event data,

the inspector

noted

an inconsistency

in the

opening time data recorded for valve SW-Y-2B.

The data taken

on May 13,

-28-

1993, for ASHE inservice testing

(IST) stroke time trending

and data

taken

on May 16,

1993, for a special test for Generic Letter 89-10

testing of motor-operated

valves differed by 12 seconds.

The inspector

noted that the timing of the valve's

opening

was controlled by an

Agastat time delay relay,

SW-RLY-V/2B5.

Consequently,

the inspector

also

examined

the periodic relay calibration records

and found that the

Agastat relay had

an as-found setting of 62 seconds,

which was proper

and consistent with the expected results.

However, the inspector

noted

that the motor-operated

valve test data recorded for the Generic Letter,

special test using

a diagnostic

computer

had recorded

a stroke time of

50 seconds;

even though the

IST test data

showed

a 62-second

timeout.

The licensee

had not investigated

the cause of this

12 second difference

between the apparent

valve stroke times for SW-V-2B.

This difference

was mentioned in the

PER 293-1319,

but had not been

pursued

by the

licensee.

During the inspection,

the licensee

prepared

PER 294-0051 to

address

the cause of the apparent difference.

The inspector

concluded that the licensee's

actions in response

to the

inspector-identified

problem appeared

to be appropriate.

Furthermore,

the inspector concluded that the licensee

should

have independently

noted

and responded

to the differences

in stroke time data.

I

Abandonment of the

SSWS

Kee -full S stem

The inspector

observed that in October

1993, the licensee

had abandoned

a nonsafety-related,

keep-full system which had served the

SSMS.

Although the system

had not been fully effective in keeping the

SSWS

full due to excessive

valve leakage,

the system

abandonment

appeared

to

coincide with the reappearance

of system waterhammer.

The assessment

performed

by the licensee

in mid-1993 concluded that the keep-full

system

was not needed for the prevention of waterhammer.

The inspector

noted that

PER 293-1319 did not address

the abandonment

of the keep-full

system in its assessment

of the recurrence of SSWS waterhammer.

The

inspector also noted that no waterhammer

events

had been recorded

from

Hay 16,

1993, until the shutdown of the keep-full system.

The licensee

stated that they would reassess

the keep-full system's

role in causing

waterhammers.

The inspector considered

the licensee's

actions to be appropriate

in

response

to the inspector's

question.

Ina

ro riate Interim PER Dis osition

In review of the event records,

the inspector noted

an interim

disposition of PER 293-1319 which did not appear

to have

a sound

technical

basis.

The interim disposition

by Systems

Engineering

compensated

for the overtraveled position of valve SW-V-2B by adjusting

the time-delay relay setting to add approximately

17 seconds

to the

original 12-second partial stroke time.

The inspector

calculated that

this would result in approximately

a 30 percent

valve opening.

This was

-29-

substantially larger than the previously successful

20 percent

opening

associated

with the 12-second

stroke time.

The inspector

was concerned that

a 30 percent

opening would

substantially

increase

flow and the chances for a waterhammer in the

SSMS.

Although, the licensee

indicated that post-modification testing

following the timing adjustment

on November 30,

1993, did not result in

a waterhammer,

the inspector

noted'that

another

waterhammer

occurred

on

December

2,

1993.

An assessment

performed

by Design Engineering after

this second

event confirmed that "...at roughly 30 to 35 percent of full

open position,

SM-V-2B can have full flow through the valve, which is

what the [plant computer] printout indicated."

The inspector

concluded

that System Engineering's

interim fix of a 17-second

opening stroke

was

not adequately

evaluated,

in that it did not prevent another

waterhammer

event.

Materhammer

Anal sis

Ca abilities

The inspector reviewed Design Engineering's

modelling of the last

waterhammer incident.

The licensee

used

a commercially-available,

computer program, "LI(T".

The program predicted

some general

trends;

however,

LI(T had not been validated for safety-related

applications

and

did not have the capability to calculate the dynamic loadings

due to

waterhammer

events.

The inspector

concluded that Design Engineering

had

developed

some capabilities to address

waterhammer,

but that the

capabilities

had not been developed to the degree that could predict

.

system performance

during

a waterhammer

event under various scenarios.

5.3.3 Conclusions

5.4

The inspector

concluded that the licensee's

examination of the

recurrence

of waterhammer in the

SSMS was not as thorough

as would be

expected

for

a repetitive problem.

The licensee

actions

appear ed to

stop short of a thorough examination

and the evaluation

appeared

to stop

at the first viable explanation of the event..

Additionally, the

licensee's

interim disposition to increase

the time of the initial valve

opening

was not adequately

evaluated

and

may have contributed to another

waterhammer

event.

Suspected

HPCS Materhammer

Event

5.4.1

Sample

and Criteria

The inspector reviewed engineering's

involvement in an event,

which

occurred at MNP-2 during the inspection,

to assess

the involvement

and

effectiveness

of engineering

support of plant activities.

Specifically,

the inspectot

reviewed

an event that was noted in the control

room log

on January ll, 1994, involving the performance of the quarterly High

Pressure

Core Spray System

(HPCS) Surveillance Test,

PPH 7.4.5. 11,

Revision

14.

-30-

5.4.2 Findings

The log entry documented

a noise the operators

had heard

and

characterized

as

a waterhammer.

The noise

was also heard in the

Radwaste

Control

Room.

The noise

was reported to have occurred

when

valves

HPCS V-10 and V-ll, in the flow test return line to the

Condensate

Storage

Tank, were closed

and the minimum flow valve,

HPCS V-

12, started to open.

The log further noted that the system

was walked

down and

no damage

was reported.

The test

was completed satisfactorily

and the system

was determined to be operable

since it met all the

requirements

of the test procedure

and

no system

damage

was evident.

Operations initiated Problem Evaluation Report

(PER)

294-0021

and

requested

that System Engineering resolve the deficiency.

The inspector reviewed the initial issue of the

PER and followed up on

engineering's

involvement in the investigation

and evaluation of the

event.

In addition, the inspector discussed

the event with the

Operations

Manager

and was briefed

by a plant support engineer,

who was

assisting

the system engineer.

5.4.3 Conclusion

5.5

The inspector

concluded that engineering

involvement during this event

was prompt, thorough,

and responsive

to the needs of the plant.

Engineering assistance

was evident,

and the appropriate

degree of

analysis

and root cause

determination

was performed.

Spray

Pond Icing

5.5.1

Sample

and Criteria

The inspector

examined the actions

taken

by the licensee

in response

to

questions

regarding

pond icing.

These questions

had

been raised

by the

NRC service water

team inspection

conducted

in February

1993,

and

documented

in NRC Inspection

Report 50-397/93-201.

~Back coood

In February

1993, the

NRC inspectors

had observed five inches of ice

covering the service water spray

ponds

and questioned

the operability of

the ponds from the standpoint of structural

adequacy

in an earthquake.

The ice had formed across

the pond

and was around the pipe supports

which supported

the spray nozzle piping rings.

It appeared

that the

weight of ice attached

to the supports

might be excessive

in a dynamic

seismic event.

The licensee

wrote Problem Evaluation

Request

(PER) 293-

140, dated February

5,

1993.

- The licensee

judged the condition to be

acceptable

and stated that

an evaluation

would be completed

by

November

1,

1993.

-'31-

5.5.2 Findings

The licensee

had closed the

PER on February

19,

1993,

based

on the

preparation of Request

For Technical

Services

(RFTS) 93-02-057 to

perform

a calculation.

The calculation

was recorded

on Calculation

Modification Record

(CMR) 93-0896,

dated October

21,

1993.

The

inspector reviewed the calculation with the cognizant structural

engineer.

The Supply System contra'cted with an outside consultant to

evaluate

the ice loading

on the pond structures.

The consultant's

report was

E(E International

Report,

"The Effect of Ice on the Support

Structures

Inside

WHP-2 Spray Ponds,"

dated October

1993.

The licensee

utilized the results of that calculation in conjunction with their own

calculations to evaluate

the effects of a seismic event

and found the

effects acceptable.

The inspector noted that the licensee

had not assessed

the worst climate

conditions for ice

and

had

assumed

that the five inches

observed

in 1993

was the worst case.

The licensee

also limited the study to

a continuous

five-inch slab of ice from pond wall-to-wall versus

forming in the

middle of the pond first near the exposed-to-atmosphere

metal piping and

structure

heat sink.

Although the inspector did not consider these

assumptions

to be conservative,

the inspector

noted that the licensee's

study was based

on

an analysis of the weakest structure in the pond,

which was conservative.

In response

to the inspector's

concern,

the l.icensee

performed

a further

study,

contacted

other agencies for historical weather information,

and

performed Calculation

CMR-94-0080,

dated January

24,

1994.

The licensee

concluded that the formation of ice was acceptable

and that the maximum

credible ice thickness,

based

on historical weather records,

was

10

inches.

The study concluded that ice would form as

a sheet,

and that

the ice would act

as

a supporting diaphragm

and would provide lateral

support to the pond structures until the ice broke due to sloshing

effects.

The sloshing effects were

seen

as breaking the ice away from

the structure leaving. a small

mass of .ice attached to the structure.

Furthermore,

the licensee

concluded that:

(1) there would only be one

cycle of sloshing which would not produce significant lateral

movement;

(2) interaction of the broken ice with the support structures

would not

be significant;

(3) the weight of ice that remained

attached to the

structure after sloshing

broke the ice would be

231 lbs. with a maximum

allowable of 400 lbs;

(4) the inertia load of the ice did not need to be

combined with the structure uplift pullout loads

due to sloshing since

the uplift and inertial loads would not occur at the

same time;

and (5)

the melting of the ice will likely occur from the edges of the pond

leaving

a potentially larger mass of ice attached

to the structure for

the period of time it takes

the ice to melt.

The inspector noted that

the licensee did not specifically analyze this case

which they concluded

would only be applicable for brief periods of time.

In addition, the

inspector

noted that the licensee

did not have

any information regarding

the licensing basis for ice considerations.

-32-

5.5.3 Conclusions

The inspector

concluded that the acceptability of the licensee's

assumptions

concerning

pond icing required further

NRC review.

The

inspector considered

that the assumptions

of ice breakage

and movement

were crucial to the licensee's

conclusions

regarding the structural

integrity of the spray

pond piping.

This issue

has

been referred to the

Office of Nuclear Reactor Regulation for further evaluation

and will be

considered

a followup item pending the

NRC evaluation.

. {Followup item 50-397/94-02-05)

No violations or deviations

were identified.

6.0

Engineering

Communications

and Programs

The .inspector

assessed

the degree

and effectiveness

of the support provided by

the Engineering

and the System Engineering organizations

to plant operations.

The inspector also

examined the status

of implementation of the licensee's

programs for personnel

and equipment

performance.

6.1

Sample

and Criteria

The inspector selected

certain

systems

and components

which had exhibited

a

history of recurring problems during the past year

and conducted

the following

activities:

Examined the historical records for the past year of plant entries

by

the responsible

system engineers,

design

system engineers,

and their

supervision

and management

to assess

whether these

persons

were spending

time in the plant assessing

the state of the plant conditions.

Examined the licensee's

system for identifying equipment

performance

problems to engineering for resolution.

Examined the licensee's

expectations for system walkdowns

by the system

engineers,

design

system engineers,

and operations staff.

Examined the licensee's

expectations

for time-in-plant for key staff

members.

Assessed

the degree of understanding

of the management

expectations

and the degree of implementation of those expectations.

Assessed

the methods

used

by the licensee's

management

to monitor the

implementation of their guidance

and assess

the effectiveness

of the

plant walkdowns.

Examined the effectiveness

of the joint walkdowns of the selected

systems'y

Engineering,- System Engineering,

and Operations.

Examined the licensee's

program for equipment

and system performance

monitoring including collecting,

analyzing,

and trending performance

data.

Determined whether minimum acceptable

performance levels

and

-33-

criteria were specified.

Assessed

whether the program effectiveness

was

periodically evaluated

by management

for needed

improvements.

The inspector

conducted

the

above examinations

by interviewing plant

operators,

shift managers,

operations

supervision

and management,

system

engineers

and their supervision

and management,

and design engineers

and their

management.

The inspector

also reviewed the administrative control

documents

and technical

documentation.

6.2

Findings

6.2. 1 System Engineering

Performance

The inspector

found that the System Engineering

and Design Engineering

. organizations

were in a state of transition.

The System Engineering

Program

had

been significantly revised beginning in October

1993 in

order to correct inadequacies

identified in the program during 1992

and

early 1993.

The revised

program provided workload adjustments

to

provide more time for the system engineers

to focus

on system

performance

and problems.

Plant

Su

ort

En ineerin

The inspector

noted that the licensee

had implemented

a particularly

important initiative with the creation of a Plant Support Engineering

staff under Design Engineering to provide additional

support for

emerging plant issue resolution,

10 CFR 50.59 safety evaluations,

and

day-to-day communications with Operations

and System Engineering.

In

preparation for changing the old program, the licensee

attended

industry

counterpart

meetings

on the subject

and conducted

information gathering

visits to their counterpart utilities for selection of successful

practices

which might be applicable to MNP-2.

Res onsibilities

The inspector

examined the

new Administrative Control Procedure,

TI 2.1,

"System Engineering," for the System Engineering

Program.

The inspector

noted that the old system engineer's

responsibilities

had

been

completely listed in a letter,

dated

November 20,

1991;

however,

the

new

procedure did not provide

a clear,

complete listing of the system

engineer's

responsibilities.

Although the licensee

had proposed certain

workload adjustments

in a letter dated

November

15,

1993,

the inspector

concluded that the system engineer responsibilities

were not clearly

specified

and communicated

in the

new procedure.

Nevertheless,

discussions

with the system engineers

and their supervision,

indicated

that there

was

a good understanding

of the responsibilities for the

program implementation.

The lack of clear communication of the system engineer's

responsibilities

did not appear to be causing

a problem because

supervision

was

so closely involved in system engineer activities.

The

- 34-

licensee

pointed out that the performance

plan for each

engineer

contained

a more complete listing of the system engineer's

expectations.

Nevertheless,

the performance

plans did not contain

a complete listing

of responsibilities.

The licensee

observed that the program was still

under development

and that the administrative control procedure

would be

evaluated

regarding the desirability of providing

a complete identi-

fication of system engineer responsibilities.

S stem Walkdowns

The System Engineering

Program provided for routine tours of the systems

at

a frequency

agreed

upon by the supervisor

and the system engineer

and

for a quarterly wal kdown by the system engineer

and responsible

personnel

from the Operations,

Haintenance

and Design Engineering

Departments.

However, the inspector

noted that the licensee

was

experiencing start-up

problems with participation in the quarterly

walkdowns from the other organizations.

The inspector

also found that there were

some missed opportunities to

include the views of other interested

organizations

in the definition of

the System Engineering

Program.

The licensee

had rank ordered the

systems

according to perceived

importance.

Both the Operations

and

System Engineering staff participated in this process.

The inspector

pointed out that this process

apparently

missed the opportunity to have

risk management

organizations

participate in the rank ordering,

an

oversight which the licensee

agreed to correct.

In addition, the

inspector

noted that the System Engineering staff had defined tour

frequency expectations

and defined the parameters

which would be

monitored

and trended to assess

system performance.

The inspector

observed that the opinions of Operations

and the risk management

organization

were not solicited in the definition of tour frequency

and

parameters

to be monitored.

The licensee

also

agreed to solicit these

opinions.

The. inspector

examined

documentation of system engineering

tours

and

concluded that tours were being performed in accordance

with agreed

upon

frequencies,

that problems

were being identified,

and system performance

parameters

were being monitored

and trended.

The inspector noted that the licensee

had established

a program for

System Engineering

management

and supervision to participate in system

tours

and impart their expectations

to the responsible

system engineers.

Supervisors

were to accompany

the engineers

on one system tour per week

and management

was to accompany

the engineers

on one tour per month.

The inspector considered this to be

a well-conceived initiative to

assure that expectations

were communicated.

However, the inspector

pointed out that it may have

been desirable for senior plant and utility

management

to have participated in the tour process to assure that the

broadest

possible perspectives

were effectively communicated

to the

system engineers.

The licensee

indicated that this comment would be

evaluated.

- 35-

Desi

n Basis

Document

Use

The inspector

asked

whether the system engineers

used the licensee's

design basis

documents

in the performance of their duties

and was

informed that the system engineers

made little use of these

documents.

The inspector noted that the documents

were not readily available

and

were only located in the supervisor's

office.

In addition, the system

engineers

and supervisor stated that the information in the documents

was not useful in the performance of their jobs.

It also

became

apparent that neither the system engineers,

nor the supervisors,

had

communicated theit

concerns

regarding the usefulness

of the information

to anyone in the engineering

organization responsible for producing the

design

documents.

The inspector considered this poor communication to

be

a missed opportunity to influence the preparation of the design

basis

documents.

Interface

Interviews of the operations staff indicated that system engineer

presence

in the pl.ant,

response

timeliness,

and credibility had

improved.

These interviews suggested

that problems regarding

System

Engineering staff stability had improved

and discussions

with System

Engineering supervision

and management

indicated that certain

initiatives were underway to improve plant presence

and stability.

These initiatives included items such

as presence

at

some shift

turnovers,

development of backup capability,

and development of a

replacement staff trainee

program for some positions.

The licensee's

program provides for performance of a joint design

system

engineer/operations/system

maintenance

engineer

walkdown, to be led by

the system engineer

nine weeks prior to the quarterly scheduled

system

outage for maintenance.

In addition, joint system walkdowns by the

same

team are conducted prior to return to power following a refueling

outage.

Status

Re orts

The licensee

had recently

begun producing

a system status report by

System Engineering

management

for Operations

and other senior

management.

The depth of system analysis

in this report was under

refinement.

~Staffin

Staffing levels in System Engineering

was discussed

with various

managers,

supervisors

and staff.

The licensee

stated that there

are

currently about

28 personnel

in the Systems

Engineering staff.

The

licensee

acknowledged that this staffing level

was at the low end of the

average for single large utility plants

and the licensee

planned to add

five-new positions in the near future to bring the staffing in line with

their current needs.

-36-

Conclusion

The inspector

concluded that the System Engineering

Program

appeared

to

have improved,

although certain oversights

in program definition were

observed.

Specifically, the inspector concluded that the procedure for

the System Engineering

Program did not provide

a clear,

complete listing

of the system engineer responsibilities,

and the expectations

of senior

management for the functions of a System Engineering

Pt ogram had not

been clearly communicated

to the mid-level managers

responsible for

developing the program

and implementing procedures.

The inspector

also

noted that additional staff needs

were being addressed,

and that

interviews with operators

indicated that system engineering

support of

plant operations

had improved.

6.2.2 Plant Performance

Monitoring and Trending Program

Performance

Monitorin

The licensee's

plant performance

monitoring program was described

in

Adminis'trative Control Procedure,

PPH 1.5.9,

Revision 5, "Plant

Performance

Monitoring Program,"

dated October

11,

1993.

The procedure

recognized

the use of the Technical Specification Testing

Program

and

the Reliability-Centered

Maintenance

Program in monitoring selected

plant systems

and equipment,

including the collection, evaluation,

and

reporting of data.

The inspector

found that this procedure did not

provide

a complete identification and coordination of all the various

parameter monitoring and trending activities performed

by the Supply

System.

For example,

the procedure

did not include the parameters

monitored

by the System Engineering

Department

and the Specialty

Programs

Group.

The inspector considered

that the lack of a well-defined program

procedure

indicated that management

had not ensured that their

expectations

had been

communicated.

Further,

the Specialty

Programs

Group was conducting

business

as specified

by informal, internally-

generated

guides without the benefit of a procedure.

The licensee

acknowledged that the performance

monitoring program would be further

assessed

and more formally integrated with the company goals

and

expectations

of management.

Reliabilit -Centered

Maintenance

RCM

Pro ram Status

The inspector discussed

the Reliability-Centered

Maintenance

(RCM)

Program with responsible

licensee

personnel.

The program consisted of

reliability-centered

maintenance

information analysis,

data obtained

from a variety of sources,

and equipment condition monitoring, (e.g.,

thermography,

vibration, oil, lubricant,

and motor current signature

analyses).

The licensee

had contacted

industry counterparts

and

EPRI during the

development of the program.

The program

was

based

upon the

EPRI process

- 37-

regarding the selection of equipment

and the preventive maintenance

tasks

which may be done to improve performance.

The methodology for

program implementation

was chiefly determined

by those activities which

were applicable to the Supply System organizations

and the existing

organizational responsibilities.

The Supply System

had obtained

EPRI

agreement

with the methodology

used to scope the program.

The licensee's

program monitored

abo'ut

1300 pieces of equipment

and

reported the results of the monitoring and trends to the System

Engineering organization for review.

The licensee

indicated that

130

systems

were scheduled

to be analyzed.

The licensee

also intended to

perform

a fault-tree analysis

on key plant equipment

and to build

component

basis files.

These files would include the kind of preventive

maintenance

done

on component

types

and

a description of the maintenance

necessary

as

a function of operating

environment

and other attributes.

The licensee

had completed

an analysis

on the Residual

Heat

Removal

and

Circulating Water

systems.

The results of these

analyses

recommended

changes

to the preventive maintenance

program

and other documents

and

programs.

The licensee

was working on methods to quickly extract

and

analyze

trended data.

Condition Honitorin

The licensee's

condition monitoring program

was specified

by

Administrative Procedure,

PPM 1.19.3,

"Condition Monitoring Program."

This program consists of process

parameter monitoring for safety-related

and balance-of-plant

(BOP) equipment.

Examples of equipment

included in

the program were safety-related

pumps,

valves, batteries,

and emergency

diesel

generators.

The

BOP monitoring included thermal-cycle monitoring

for the Service

Water, Circulating Water,

and Fuel

Pool Cooling systems.

The program also included heat exchanger monitoring (thermal

performance

and pressure

drop testing),

thermography,

vibration monitoring, oil

analysis,

and motor current signature

analysis.

~Trendin

The trending program trended

almost all of the parameters

collected

by

the various organizations

in the conduct of the performance monitoring

program;

prepared

trend plots covering three

month or three year periods

depending

upon the frequency of data collection;

and distributed the

trended information to system engineers,

operations

and others.

Special

reports

on potential

problems

were issued

as warranted.

For example,

a

special

report described vibration anomalies

on Reactor Recirculation

Pump

1A, suggested

the possible existence of a small

pump shaft crack,

and provided recommendations

to avoid propagation

along with additional

monitoring suggestions.

Conclusions

Although the licensee's

plant performance monitoring and trending

programs

were generally developing

adequately,

the inspector

concluded

-38-

that they could have

been better defined

and did not fully reflect the

expectations

of management.

For example,

the program administrative

control document did not address

all of the various performance

monitoring activities being performed

and certain monitoring activities

were being performed without benefit of a approved

procedure.

6.2.3 Design Engineering Effectiveness

The inspector

held discussions

with the Director of Engineering,

the

Manager of Design Engineering,

.and several

of their staff.

The

inspector

found that Engineering

had

an extensive

number of improvement

initiatives in various stages

of completion

and concluded that

completion of these

could only improve the effectiveness

of engineering

support of operations.

Each initiative was assigned

a responsible

manager

and appeared

to be updated

in status regularly.

Plant Trackin

Lo

As an example of'mprovement,

in late October

1993,

Engineering

achieved

zero overdue

items

on the plant tracking log, indicating that emergent

work and backlogs

were being effectively managed.

In addition, the zero

overdue item condition had continued since achieving that milestone.

To better understand

what was in the plant tracking log (PTL) and

how it

was being used,

the inspector requested

a list of all the open

engineering

items in the

PTL and several

specific items representing

engineering

work that was due to be completed during the period of

January

17-28,

1994.

The inspector

used these lists in discussions

with

'various engineering

managers

and supervisors

to obtain

an understanding

as to how the

PTL was

used

and 'how various departments

tracked their

workloads

and determined their resource

requirements.

The inspector

determined that:

The

PTL was not very interactive or user friendly. It had not

been

used

as the primary tracking tool, nor had it been

used for

determining resource

needs.

Specific subsets

of open items,

which

were sorted

by name

and due dates,

were used.

In addition, other

status tools

had

been developed

by individual departments

for

their individual monitoring.

Engineering

managers

and supervisors

were keenly aware of open

action items for which they were responsible.

The inspector

noted that the Engineering

Improvements

Document,

which listed several

enhancements

and improvements

(either

planned,

in progress,

or completed)

included

a guality Action Team

(OAT) which had completed the development of an enhanced

action

item tracking system to replace the

PTL.

The licensee

stated that

the (AT results

were being reviewed

and

a plan was under

development to implement the proposed

changes.

39-

En ineerin

Backlo

The inspector

held discussions

with the Design Engineering

Manager

and

several

individuals who were closely involved with the request for

engineering technical

services

(RFTS) backlog reduction efforts.

The

inspector determined that,

as of July 1992, there were about

2500 items

in the backlog.

The licensee

had perfor'med

an initial comprehensive

review to define the content.

The inspector

examined the results of the

licensee's

comprehensive

review, the methods of accomplishment,

and the

documented results.

In summary,

the backlog

was determined to consist

of about

70 percent active tasks

and future work.

About 10 percent

were

items that were essentially

complete,

but needed

closure documentation.

About three percent

were abandoned

tasks

and required purging.

The

balance

consisted of drawings needing corrections,

unassigned

tasks,

and

long-range planning work.

The licensee

performed

a second

comprehensive

review in July 1993 of about

850 remaining

items that were set

up prior

to July 1991 using similar criteria.

About 50 percent

were drawing

corrections,

and the balance

were active work or candidates

for closure.

The inspector concluded that

a significant effort had

been

conducted to

manage the work backlog

and that Engineering

had been successful

in

reducing the backlog to the current level of about

1100

RFTS.

The

majority of the items closed

represented

real work, with relatively few

categorized

as

abandoned

or redundant

items.

The inspector also noted

that the reduction efforts did not result in stifling the generation of

new RFTS,

as is sometimes

experienced

in backlog reduction programs.

The inspector considered this indicative of a well-managed

program.

Benchmarkin

Initiatives

The inspector reviewed the results of the licensee's

Benchmarking

Initiatives Program,

which was

an effort to become

more aware of

industry initiatives and good practices

by visiting other sites that

have

been cited

as good performers in selected

areas,

such

as

system

engineering

and commitment tracking.

The licensee

used the information

from these

benchmarking trips to determine

a starting point for

developing

improved practices

both in the Engineering

Department

and in

other plant organizations.

The benchmarking trips were

made

by key

managers,

supervisors,

and staff.

The inspector also noted that there

had

been significant involvement by the licensee's

staff in outside

committee activities

and meetings.

An example of a recent

benchmarking

trip was

a December

1993 visit by the Hanager of Technical

Services to

the Monticello and Callaway nuclear

power plants to review their System

Engineering

Programs.

0 erations

Interface with Desi

n

En ineerin

Interviews with Operations

Department

personnel

indicated

a lower degree

of satisfaction with the effectiveness

of Design Engineering

support

than

had been

expressed

for System Engineering.

Improvement

-40-

opportunities

suggested

by the operations staff included getting more

and earlier operations

input into design

change

planning,

spending

more

time in the plant so

as to better preclude interference

problems,

improving communications with the operators

and operations staff,

and

speeding

up the minor modification process.

The licensee

had recently

embarked

upon

a program to speed

up the minor modification process.

The inspector's

discussions

with Engineering

personnel

indicated that

they were not aware that operations

did not view the efforts of the

Engineet ing organization in accordance

with their own opinion of the

effectiveness

of their operations

support.

The inspector

observed that

the expectations

of the licensee's

senior management

regarding

engineering

support for operations

were not clearly defined

and

communicated to the Engineering organization.

In some cases,

the

inspector

found that Engineering

Department

personnel

did not clearly

identify their support activities to the operations

management

and

staff.

These

two situations contributed to the disparity of views

regarding the effectiveness

of engineering

support for operations.

The

licensee

indicated that expectations

would be assessed

and communicated

to improve relationships

between

the two organizations.

Subsequent

to these discussions,

the inspector

was informed that the

licensee

began holding periodic staff lunches.

The purpose of these

lunches

was to provide the plant staff with information regarding the

role of Design Engineering

and their current activities.

A selected

cross section of plant personnel

were invited to the sessions,

and

opportunities

were provided for questions.

According to the licensee,

these

sessions

generated

good questions

and

a better understanding

of

the role of Design Engineering

and their activities.

The licensee

stated that they planned to continue the periodic lunches.

Conclusion

The inspector

concluded that the various Engineering

improvement

initiatives that were in progress

or planned

should

improve the

effectiveness

of engineering

support for the operation of the plant.

Specifically, the work that

had

been

done

on reducing the significant

backlog of RFTS and other work had already

had significant impact.

The

backlog reduction also demonstrated

Engineering's willingness to improve

their effectiveness

in response

to plant needs.

Furthermore,

the site's

benchmarking activities, which included visits to other sites with

successful

programs,

appeared

to be effective in improving performance

in key areas

such

as system engineering.

The licensee's

increased

involvement in external

committee activities appeared

to improve focus

on ongoing industry initiatives.

Nevertheless,

the inspector

concluded

that it was too early to assess

long term effectiveness

of these

initiatives, but encouraged

the licensee to continue their attention to

the improvement initiatives.

The inspector also noted that licensee

management

had not established

an agreed

upon set of expectations

to

assure

the effectiveness

of Design Engineering interface with Operations

or System Engineering.

6.2.4 Project Nanagement Activities

The licensee

had recently established

a group dedicated

to assuming

project management

responsibilities for plant modifications

and selected

major maintenance

tasks.

The group was called

"WNP-2 Projects",

and

reported to the Assistant

Hanaging Director for Operations.

The

licensee

stated

the group was formed to provide

an adjustment to the

system engineer

workload and to provide better

management

and

coordination of major plant work efforts.

A responsibility document

and

charter

had

been drafted

and agreed to by senior

management.

Daily

implementation of the charter

had

been the subject of informal table-top

guides,

describing

how the project management

functions were to be

accomplished.

The formal functional procedures

for the organization

had

not yet been issued.

The licensee

stated that the project management

team

had

been envisioned

to include system engineering,

maintenance,

health physics,

design

engineering,

operations,

outage

management,

work planners,

schedulers,

estimators,

and site support craft representatives.

The team output was

envisioned to be

a project proposal to the Plant Review Committee

(PRC)

for the

PRC to set priorities and approve

implementation.

The inspector

suggested

that, in addition to the normal Operations

Department

individual responsible for design

change interface,

the licensee

consider inclusion of the various Operations

Department individuals who

were expert in and responsible for the particular

system involved in a

particula} design

change

in order to improve the quality of the

Operations

Department contribution.

The licensee

stated that they

recognized

the potential

improvement

and would consider its

implementation.

6.2.5 Design Basis

The inspector reviewed the adequacy of the procedures for the generation

of Design Requirements

Documents

(DRDs),

sampled

DRDs to assess

the

accuracy

and completeness

of information they contained,

and assessed

the perceived

usefulness

of the

DRDs through interviews with licensee

personnel.

Validation and Verification of Desi

n

Re uirements

Documents

The licensee's

DRD program included

DRD preparation,

design

database

review and reconstitution,

DRD verification and validation,

and

documentation

and resolution of open items.

The procedure

which defined

the processes

to be followed in developing the Design Requirements

Documents

was

EDP 2.23,

"Preparation of Design Requirements

Documents,"

Revision I, dated October

1,

1993.

The inspector considered

that the

procedure satisfactorily addressed

all of the above items.

However, the

inspector

noted that prior to July 1,

1993,

Engineering

Standard

PDS-6,

"Design Requirements

Document

Program Description

and Writer's Guide,"

outlined the

DRD Program

Plan

and defined the structure

and format of

documents written to consolidate

the design

bases

and requirements

of

'

42

WNP-2 systems

and specialty subjects.

Since

DRDs are part of MNP-2

Design Specifications,

the relevant procedure

EI 2.3,

"Preparation

and

Revision of MNP-2 Design Specifications,"

which delineated

responsibilities,

was also applicable.

The inspector

was concerned

that procedure

PDS-6 (which was

no longer

applicable)

was weak in specifying the requirements for the licensee's

DRDs.

This was of concern

because

the procedure

was

used to develop

a

majority of the

DRDs and the licensee

did not intend to revise these

older

DRDs to the requirements

of their current procedure.

An example

of the weakness

of the older

DRD procedure

was the validation

(comparison to the physical plant configuration)

and verification

(correct transfer of information from source

documents

into DRDs)

processes.

Although there

was

a requirement in PDS-6 for DRD

validation, the procedure

did not describe

the details of how such

a

validation should

have

been

accomplished.

The inspector

found that this

generally resulted in a lack of a detailed validation of approximately

90 percent of the

DRDs generated prior to implementing the

new

procedure,

EDP 2.23.

The licensee

had

an open issue regarding the

adequacy of the validation of the

DRDs produced

under

PDS-6 in their

Revised

DRD Program Plan,

dated

December

15,

1993.

The licensee's

action appeared

to be appropriate.

Omissions

Noted in Desi

n

Re uirement

Documents

The inspector identified some omissions in Design Requirement

Document

(DRD) 309,

"Standby Service Mater System."

For example,

DRD 309 did not

clearly refer to an important calculation for system design

(Calculation

HE-02-91-41) which calculated

SSWS flows and temperatures.

DRD 309 was

limited to referenced

Calculation HE-02-92-43,

which only computed

room

temperatures

based

on room heat loads.

In addition,

DRD 309 described

the requirement for the time-dependent

opening of valve SM-V-2A(2B) to

prevent

SSMS waterhammer.

However, the

DRD did not provide the basis

for the time dependent profile.

Conclusions

6.3

The inspector

found the license's

Design Requirement

Document

Program

.documents

did not contain information sufficient to make them useful to

plant users.

In addition, the validation

and verification process

used

for the DRD's resulted

in varying amounts

and types of validation

and

verification.

As discussed

in Section 6.2. 1 of this inspection report,

the inspector also found that the system engineers

made little use of

the design basis

documents primarily due to the lack of details in those

documents.

Conclusions

The inspector concluded that the degree

and effectiveness 'of the support

provided by the Engineering Directorate

and the System Engineering

organizations

for plant operations

was clearly improving.

This was evidenced

43

by obs'erved

improvements

in the implementation of the licensee's

programs for

personnel

and equipment

performance.

The inspector also concluded that System

Engineering

appeared

to have

improved although certain oversights

in program

definition were observed.

Additional staff needs

were being addressed,

and

interviews with operators

indicated that System Engineering support of plant

operations

had improved.

Also, the inspector

concluded that the licensee's

plant performance

monitoring

and trending programs

could have

been better

managed,

and that they did not

appear to have

had the benefit of the guidance

and expectations

of senior

management.

For example,

the program administrative control

document did not

address all of the various performance monitoring activities being performed

and certain monitoring activities were being performed without benefit of a

approved

procedure.

The inspector also considered

that the various Engineering

improvement

initiatives that were in progress

or planned

should

improve the effectiveness

of engineering

support for the operation of the plant.

Specifically, the work

that

had

been

done

on reducing the significant backlog of RFTS's

and other

work had already

had significant impact.

The backlog reduction also

demonstrated

Engineering's willingness to improve their effectiveness

in

response

to plant needs.

Furthermore,

the site's

benchmarking activities,

which included visits to other sites with successful

programs,

appeared

to be

effective in improving performance

in key areas

such

as system engineering.

The licensee's

increased

involvement in external

committee activities appeared

to improve focus

on ongoing industry initiatives.

Although the inspector

observed that it was too early to assess

long term effectiveness

of those

initiatives, the licensee

was encouraged

to continue their attention to the

improvement initiatives.

The inspecto'r also noted that licensee

management

had not'established

an agreed

upon set of expectations

to assure

the

effectiveness

of Design Engineering interface with Operations

or System

Engineering.

No violations or deviations

were identified.

7.0

Licensee Self Assessment

7.1

guality Assurance

Oversight

7.1.1

Sample

and Criteria

The inspector

examined the activities of the guality Assurance

(gA)

organization in the oversight of engineering

effectiveness.

The quality

assurance

organization

had performed

about

20 audits

and surveillances

during the past

18 to 20 months looking at the broad

area of engineering

support of operations.

7.1.2 Findings

The inspector

found that the

gA organization audits

had identified

several

penetrating

findings with a lower rate of findings during the

most recent time frame.

The licensee

stated that the recent lower rate

of findings was due to the 'fact that the last six-month period consisted

of mostly steady-state

power operation with little opportunity for

extensive engineering interface with operations.

The

gA activities

indicated that:

Design Engineering

had improved in their understanding

of Project Modification Request technical

requirements;

communications

with operations

had improved slightly; improvement

was needed

in

engineering participation in the de'finition of post-modification

testing;

and there

was

a lack of consistency

in the quality of the

engineering interface with operations

due, in part, to loosely defined

management

expectations

and administrative controls.

The inspector subsequently

conducted

an additional review of several

Technical

Assessments,

gA Surveillances

and

a gA Audit listed below:

TA 92-015,

Set Point Program

Review

TA 92-017,

MOV Program Implementation Yerification

TA 93-001,

Assessment

of Long Term Corrective Actions 'for Core

Instability Event.

TA 93-003,

Technical

Communication

between

Engineering

and

Operations.

TA-93-004, Design Review of Selected

R-8 Outage Modifications.

SR 292-0038,

SW Expansion Joint Adjustment

SR 292-0088,

Design

and Inst of ECCS

Pump

Room Seals

SR 293-0027,

Safety System Modification Adequacy for R-8

'R 293-0038,

8/93 Forced

Outage

and Startup Oversight Activities.

gA Audit 93-612, Corrective Action Program, Specifically

Procedural

Adherence.

En ineerin

Res onsibilit Clarification

The inspector reviewed Technical

Assessment

(TA) 93-04, in which the

gA

Department

performed

a review of selected

modifications scheduled for

implementation during the eighth refueling outage.

The assessment

found

that the design control process

was adequate

and, resulted

in acceptable

design

change

packages.

However,

the assessment

also stated that Design

Engineering's

input to post-modification testing

(PMT) requirements

was

minimal, and should

be increased.

(}uality Finding Report

((FR)

No. 93-

001 was issued to Engineering

on January

26,

1993, to document the

finding.

Design Engineering's

response

to the problem,

which was included in TA

93-04, stated that,

"Presently there is no requirement for Design

Engineering to specify or review normal

acceptance

criteria.

There is

a

perceived deficiency that Design Engineering

should document

and specify

all required Post-Modification Testing requirements."

Programs

and

Audits accepted

the Design Engineering

response.

They recorded their

rationale for acceptance

in the technical

assessment

which stated

the

response

was acceptable:

"...because

adequate

PMT was actually performed

even though Design Engineering's

involvement

was minimal

and

undocumented."

45-

The inspector noted that Engineering Instruction,

EI 2.8,

"Generating

Facility Design

Change

Process,"

Revision 7, dated

February 8,

1989,

required Design Engineering to provide post-modification test

requirements.

Specifically, Section 3.1, Action 16, stated that,

"Cognizant

and Participating Engineer... If installation, functional or

performance test requirements

need to be'considered,

prepares

a Test

Requirement

Summary in accordance

with Attachment 5.5 and includes

[Basic Design

Change]

BDC."

The Test Requirement

Summary is described

as requiring the inclusion of the test acceptance

criteria.

As

a result of this concern,

the licensee

determined that

a procedure

clarification was required to clearly specify what test

acceptance

criteria should

be provided by Design Engineering.

The licensee

also

stated that they intended to revise

EI 2.8 to clarify the test

requirements.

7.1.3 Conclusions

The inspector considered that the assessments,

surveillances

and audits

were thorough, insightful,

and contained

good findings and

recommendations.

The inspector also noted that the audits

had

been

responded

to in a generally timely manner

and that the responses

appeared

adequate.

The inspector

noted that completed actions

were

being reviewed

and verified by the

gA organization.

No violations or deviations

were identified.

8.0

Exit Neeting

On January

28; 1994, the inspector

met with licensee

representatives

(as noted

in Section 3.0) to discuss

the inspection findings.

The licensee

did not

identify as proprietary

any of the materials discussed

with or reviewed by the

inspectors

during this inspection.