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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17292B7421999-07-20020 July 1999 LER 99-001-00:on 990628,ESF Signal Closed All Eight MSIVs While Plant Was Shutdown.Caused by Failure of Relay RPS-RLY-K10D.Subject Relay Was Replaced & Tested on 990630. with 990720 Ltr ML17292B4451998-10-27027 October 1998 LER 98-012-01:on 980715,failure to Comply with Requirements of TS SR 3.8.4.7 Was Noted.Caused by Inadequate Work Practices.Training Session Was Held with Personnel.With 981027 Ltr ML17284A7561998-09-0303 September 1998 LER 98-013-00:on 980805,ESF Actuations Were Noted Due to Deenergization of Vital Electrical Bus SM-8.Caused by Inadequate Direction in Troubleshooting Plan.Will Conduct Training for Engineering Personnel.With 980903 Ltr ML17284A7571998-09-0202 September 1998 LER 98-014-00:on 980807,completion of TS 3.8.1.F Required Shutdown Due to Inoperability of EDG-2 Was Noted.Caused by Degraded Voltage Regulator for DG-2.Replaced Voltage Regulator & Associated Scrs.With 980902 Ltr ML17284A7551998-09-0202 September 1998 LER 98-015-00:on 980808,discovered Reactor Coolant Pressure Boundary Leak During Shutdown Conditions.Caused by Leakage from Socket Weld (Fwb 63) on Elbow Connection.Failed Piping Connection Was Replaced.With 980902 Ltr ML17284A7311998-08-17017 August 1998 LER 98-012-00:on 980716,determined That 24-month SR 3.8.4.7 Had Not Been Fulfilled within Specified Frequency.Caused by Inadequate Work Practices.License Requested & Received Enforcement Discretion Re Battery Svc test.W/980817 Ltr ML17284A7121998-07-23023 July 1998 LER 98-006-01:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of 10CFR50,App R Calculations for High Impedance Faults.Caused by Inadequate Work Practices.Implemented Procedural Changes ML17284A6951998-07-17017 July 1998 LER 98-011-00:on 980617,ECCS Pump Room Flooding Was Noted Due to FP Sys Pipe Break.Caused by Inadequate Design of FP Sys.Detailed Review of FP Sys Design Was Conducted. W/980717 Ltr ML17284A6961998-07-15015 July 1998 LER 98-010-00:on 980615,TS Required Shutdown Due to Inoperability of TIP Sys Isolation Valve Was Noted.Caused by Improper Installation of TIP Tubing.Reattached Affected Tubing & Inspected Other TIP tubing.W/980715 Ltr ML17284A6731998-07-0101 July 1998 LER 98-009-00:on 980606,nuclear Steam Supply Shutoff Sys Group 3 & 4 Isolations During Testing Was Noted.Caused by Procedural Deficiency.Counseled Individuals Involved in preparation.W/980701 Ltr ML17284A6651998-06-24024 June 1998 LER 98-007-00:on 980530,inadvertent Full Scram & Division 1 ECCS Injection Was Noted.Caused by Failure to Meet Mgt Work Practice Expectation When Encountering Deficient Procedure. Incident Review Board Convened to Review event.W/980624 Ltr ML17284A6641998-06-24024 June 1998 LER 98-008-00:on 980531,inadvertent Full Scram During RPV Leak Testing in Mode 4 Was Noted.Caused by Change in Mgt Techniques.Revised Procedures to Take Into Account Addl Water Head in Pressure Sensing lines.W/980624 Ltr ML17284A6631998-06-19019 June 1998 LER 98-006-00:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of App R Calculations for High Impedance Fault Analysis.Caused Indeterminate. Implemented Procedural Changes Involving Operator Action ML17284A6551998-06-0404 June 1998 LER 98-005-00:on 980506,potential for Failure of RHR Sys Valve to Close on Isolation Signal Was Noted.Caused by Design Deficiency.Caution Tag Was Placed on RHR-V-40 Control Switch to Inform Plant Operators of limitation.W/980604 Ltr ML17284A6421998-06-0101 June 1998 LER 98-004-00:on 980502,determined That Primary Containment Penetration Overcurrent Protection Does Not Meet Reg Guide 1.63 Requirements.Caused by Inadequate Design Changes. Installed Addl Fuse in RHR-MO-9 circuit.W/980601 Ltr ML17292B3281998-04-0909 April 1998 LER 98-002-00:on 980311,reactor Scram & Plant Transient Occurred,Due to Failed Closed Main Steam Isolation Valve. Caused by Loss of Pneumatic Actuating Supply Pressure. Problem Evaluation Request Written for Failure of MS-V-22D ML17292B3291998-04-0909 April 1998 LER 98-003-00:on 980311,WNP-2 Experienced SCRAM Signal as Result of Low Rpv.Caused by Less than post-SCRAM Operational Strategy for Resetting SCRAM Signal in Conditions.Changes in post-SCRAM Operational Strategy implemented.W/980409 Ltr ML17292B2661998-03-0404 March 1998 LER 98-001-00:on 980203,automatic Start of HPCS EDG Was Noted.Caused by Operator Error.Operations Crew Stabilized Plant at Approximately 75% Reactor Power & Investigation of Event Was initiated.W/980304 Ltr ML17292B1111997-11-10010 November 1997 LER 97-011-00:on 971010,HPCS Battery Charger Failed.Caused by Failure of a Phase Firing Control Circuit Board Due to Aging During 7 Yrs of Use.Hpcs Sys Was Immediately Declared inoperable.W/971110 Ltr ML17292B1151997-11-0707 November 1997 LER 97-010-00:on 970906,discovered That TS SR 3.4.5.1 for Identified Portion of RCS Total Leakage Would Not Be Able to Perform within Time Limits of SR 3.0.2.Caused by Inadequate Methods.Method of Meeting SR 3.4.5.1 Established ML17292B0641997-09-24024 September 1997 LER 97-004-01:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Indication of Entry Into Region a of power-to-flow Map.Caused by Inadequate Attention to Detail.Established Event Evaluation teams.W/970924 Ltr ML17292B0241997-08-18018 August 1997 LER 97-009-00:on 970717,discovered Error in Recently Performed Inservice Testing procedure,OSP-TIP/IST-R701. Caused by Procedure Inadequacy.Plant Procedure OSP/TIP/IST-R701 Will Be changed.W/970818 Ltr ML17292B0291997-08-15015 August 1997 LER 97-008-00:on 970716,wire Seal Used to Lock Containment Instrument Air Pressure Control valve,CIA-PCV-2B,found Not Intact.Cause of Misadjustment of CIA-PCV-2B Unknown.Event Will Be Communicated to Plant employees.W/970815 Ltr ML17292B0201997-08-15015 August 1997 LER 97-S01-00:on 970718,failure to Take Compensatory Measure for Inoperative Microwave Security Zone Occurred. Caused by Personnel Error.Training Will Be Conducted W/ Appropriate Members of Security force.W/970815 Ltr ML17292A9481997-07-23023 July 1997 LER 97-007-00:on 970611,voluntary Rept of Automatic Start of DG-1 & DG-2 Was Experienced.Caused by Undervoltage Condition on Electrical Busses SM-7 & SM-8.Circulating Water Pump CW-P-1C Control Switch Placed in pull-to-lock.W/970723 Ltr ML17292A9201997-06-26026 June 1997 LER 97-006-00:on 970527,non-performance of Surveillance Requirement 3.6.1.3.2 for Blind Fanges,Was Noted.Caused Because Misunderstanding of Intent of Specs.Added Five Structural Assemblies for SP.W/970626 Ltr ML17292A8331997-04-28028 April 1997 LER 97-004-00:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Entry Into Region a of power-to-flow Map Following Planned Trip of Single Mfp. Event Evaluation teams,established.W/970428 Ltr ML17292A8311997-04-28028 April 1997 LER 97-005-00:on 970327,valid Reactor Scram Signal Received Due to Low Water Level Condition During Preparations for SRV Testing.Caused by Risks & Consequences of Decisions Not Completely Identified.Restored Water level.W/970428 Ltr ML17292A8251997-04-21021 April 1997 LER 97-003-00:on 970320,notification of Noncompliance W/Ts as TS SRs for Response Time Testing Were Not Being Met for Specified Instrumentation in Rps,Pcis & Eccs.Requested Enforcement Discretion for One Time exemption.W/970421 Ltr ML17292A7431997-03-20020 March 1997 LER 97-002-00:on 970218,determined That Rod Block Monitor (RBM) Calibr Values Were Not Set IAW Tech Specs.Caused by Calibr Procedures Inadequacies.Revised & re-performed RBM Channel Calibr procedures.W/970330 Ltr ML17292A7401997-03-13013 March 1997 LER 97-001-00:on 970211,reactor Water Cleanup Sys Blowdown Flow Isolation Setpoint Was Slightly Above TS Allowable Valve Occurred Due to Calculation Error.Lds Fss LD-FS-15 LD-FS-16 Were Declared inoperable.W/970313 Ltr ML17292A6641997-01-22022 January 1997 LER 96-009-00:on 961220,miscalculation of Instantaneous Overcurrent Relay Settings Resulted in Inoperability of safety-related Equipment.Caused by Utilization of Inappropriate Design.Testing Was completed.W/970122 Ltr ML17292A6461997-01-0606 January 1997 LER 96-008-00:on 961205,failure to Comply with TS Action Requirement for Emergency Core Cooling Sys Actuation Instrumentation Occurred Due to Unidentified Inoperability Condition.Pmr initiated.W/970106 Ltr ML17292A6371996-12-19019 December 1996 LER 96-007-00:on 961122,electrical Breakers Were Not Seismically Qualified in Test/Disconnect Position.Circuit Breaker Mfg Did Not Consider Raced Out Breaker Position During Testing.Relocated Circuit breakers.W/961217 Ltr ML17292A4121996-08-0808 August 1996 LER 96-006-00:on 960709,average Power Range Monitor Rod Block Downscale Surveillance Not Performed Prior to Entry Into Mode 1.Caused by long-standing Misinterpretation of Requirements of Tss.Procedures revised.W/960808 Ltr ML17292A3801996-07-24024 July 1996 LER 96-004-00:on 960624,plant Was Manually Scrammed by Control Room Personnel Due to Reactor Water Level Transient Experienced During Testing of Digital Feedwater Sys.Caused by Programming Error.Sys Was corrected.W/960724 Ltr ML17292A3771996-07-24024 July 1996 LER 96-005-00:on 960624,determined Missed Surveillance Test Re Channel Check of Average Power Range Monitor.Caused by Inadequate Procedures.Revised Surveillance Procedure Re When APRM Checks Must Be performed.W/960724 Ltr ML17292A3641996-07-12012 July 1996 LER 96-003-00:on 960615,required Surveillance Test Not Performed When Required by TS 3.4.1.3.Caused by Inadequate Procedures.Implementing Surveillance Procedure & Reactor Plant Startup Procedures revised.W/960712 Ltr ML17292A3361996-06-20020 June 1996 LER 96-002-00:on 960504,critical Bus SM-8 Lost Power When Supply Breaker 3-8 Tripped.Caused by Personnel Error. Operators Counselled & Procedures revised.W/960620 Ltr ML17292A2861996-05-24024 May 1996 LER 96-001-00:on 960425,inadvertent ESF Actuations Occurred Due to Tripping of Temporary Power Supply to IN-3.Caused by Personnel Error.Operations Restored to IN-3 Loads & Reset ESF actuations.W/960524 Ltr ML17291B0891995-10-19019 October 1995 LER 95-011-00:on 950919,failed to Comply W/Ts SR for RCIC Sys Due to Analysis Deficiency That Resulted in Inadequate Surveillance Test Procedure.Surveillance Procedure Revised to Correct deficiency.W/951019 Ltr ML17291A9021995-07-0707 July 1995 LER 95-010-00:on 950609,HPCS DG Declared Inoperable Due to Discovery That TS Test Method Incomplete.Caused by Inadequate Testing Procedure.Test Procedure for HPCS DG Reviewed & Special Test Procedures written.W/950707 Ltr ML17291A9031995-07-0707 July 1995 LER 95-009-00:on 950607,inadvertent MSIV Closure Occurred During Surveillance Test Due to Poor Communication Between Test Team.Determined That MSIV Closure Not Valid Because Closure Not Triggered by Plant conditions.W/950707 Ltr ML17291A8501995-06-0808 June 1995 LER 95-006-01:on 950405,reactor Scram Occurred During Surveillance Testing Due to Protective Sys Relay Failure. Replaced Failed Relay Before Plant Startup ML17291A8101995-05-12012 May 1995 LER 95-008-00:on 940125,TS Wording Lead to Potential TS Violation.Caused by Lack of Clarity in Ts.Submitted Improved TS for Plant to Provide Addl clarity.W/950512 Ltr ML17291A7841995-05-0505 May 1995 LER 95-007-00:on 950222,emergency Diesel Start Occurred Due to Voltage Transient on BPA Grid.Confirmation Was Received at 17:51 H That Disturbance Had Originated in BPA Grid ML17291A7801995-05-0404 May 1995 LER 95-006-00:on 950405,main Turbine Trip Occurred During Performance of Surveillance Test Due to Protective Sys Relay Failed.Replaced Failed Relay Before Plant startup.W/950504 Ltr ML17291A7851995-05-0303 May 1995 LER 95-005-00:on 950222,inoperable IRM Had Been Relied Upon to Meet TS Requirements During Reactor Startup.Caused by Lack of Neutron Source to Test Instrumentation. Sys Knowledge Gained Will Be incorporated.W/950503 Ltr ML17291A7071995-03-25025 March 1995 LER 95-004-00:on 950226,malfunction in Main Turbine DEH Control Sys Caused All Four High Pressure Turbine Governor Valves to Rapidly Close.Caused by Blown Fuse.Suspected Faulty Circuit Card replaced.W/950325 Ltr ML17291A7011995-03-20020 March 1995 LER 95-002-00:on 950218,automatic Reactor Scram Occurred. Caused by Erroneous Positioning of Control During Performance of Scheduled Periodic Functional Test.Control repositioned.W/950320 Ltr 1999-07-20
[Table view] Category:RO)
MONTHYEARML17292B7421999-07-20020 July 1999 LER 99-001-00:on 990628,ESF Signal Closed All Eight MSIVs While Plant Was Shutdown.Caused by Failure of Relay RPS-RLY-K10D.Subject Relay Was Replaced & Tested on 990630. with 990720 Ltr ML17292B4451998-10-27027 October 1998 LER 98-012-01:on 980715,failure to Comply with Requirements of TS SR 3.8.4.7 Was Noted.Caused by Inadequate Work Practices.Training Session Was Held with Personnel.With 981027 Ltr ML17284A7561998-09-0303 September 1998 LER 98-013-00:on 980805,ESF Actuations Were Noted Due to Deenergization of Vital Electrical Bus SM-8.Caused by Inadequate Direction in Troubleshooting Plan.Will Conduct Training for Engineering Personnel.With 980903 Ltr ML17284A7571998-09-0202 September 1998 LER 98-014-00:on 980807,completion of TS 3.8.1.F Required Shutdown Due to Inoperability of EDG-2 Was Noted.Caused by Degraded Voltage Regulator for DG-2.Replaced Voltage Regulator & Associated Scrs.With 980902 Ltr ML17284A7551998-09-0202 September 1998 LER 98-015-00:on 980808,discovered Reactor Coolant Pressure Boundary Leak During Shutdown Conditions.Caused by Leakage from Socket Weld (Fwb 63) on Elbow Connection.Failed Piping Connection Was Replaced.With 980902 Ltr ML17284A7311998-08-17017 August 1998 LER 98-012-00:on 980716,determined That 24-month SR 3.8.4.7 Had Not Been Fulfilled within Specified Frequency.Caused by Inadequate Work Practices.License Requested & Received Enforcement Discretion Re Battery Svc test.W/980817 Ltr ML17284A7121998-07-23023 July 1998 LER 98-006-01:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of 10CFR50,App R Calculations for High Impedance Faults.Caused by Inadequate Work Practices.Implemented Procedural Changes ML17284A6951998-07-17017 July 1998 LER 98-011-00:on 980617,ECCS Pump Room Flooding Was Noted Due to FP Sys Pipe Break.Caused by Inadequate Design of FP Sys.Detailed Review of FP Sys Design Was Conducted. W/980717 Ltr ML17284A6961998-07-15015 July 1998 LER 98-010-00:on 980615,TS Required Shutdown Due to Inoperability of TIP Sys Isolation Valve Was Noted.Caused by Improper Installation of TIP Tubing.Reattached Affected Tubing & Inspected Other TIP tubing.W/980715 Ltr ML17284A6731998-07-0101 July 1998 LER 98-009-00:on 980606,nuclear Steam Supply Shutoff Sys Group 3 & 4 Isolations During Testing Was Noted.Caused by Procedural Deficiency.Counseled Individuals Involved in preparation.W/980701 Ltr ML17284A6651998-06-24024 June 1998 LER 98-007-00:on 980530,inadvertent Full Scram & Division 1 ECCS Injection Was Noted.Caused by Failure to Meet Mgt Work Practice Expectation When Encountering Deficient Procedure. Incident Review Board Convened to Review event.W/980624 Ltr ML17284A6641998-06-24024 June 1998 LER 98-008-00:on 980531,inadvertent Full Scram During RPV Leak Testing in Mode 4 Was Noted.Caused by Change in Mgt Techniques.Revised Procedures to Take Into Account Addl Water Head in Pressure Sensing lines.W/980624 Ltr ML17284A6631998-06-19019 June 1998 LER 98-006-00:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of App R Calculations for High Impedance Fault Analysis.Caused Indeterminate. Implemented Procedural Changes Involving Operator Action ML17284A6551998-06-0404 June 1998 LER 98-005-00:on 980506,potential for Failure of RHR Sys Valve to Close on Isolation Signal Was Noted.Caused by Design Deficiency.Caution Tag Was Placed on RHR-V-40 Control Switch to Inform Plant Operators of limitation.W/980604 Ltr ML17284A6421998-06-0101 June 1998 LER 98-004-00:on 980502,determined That Primary Containment Penetration Overcurrent Protection Does Not Meet Reg Guide 1.63 Requirements.Caused by Inadequate Design Changes. Installed Addl Fuse in RHR-MO-9 circuit.W/980601 Ltr ML17292B3281998-04-0909 April 1998 LER 98-002-00:on 980311,reactor Scram & Plant Transient Occurred,Due to Failed Closed Main Steam Isolation Valve. Caused by Loss of Pneumatic Actuating Supply Pressure. Problem Evaluation Request Written for Failure of MS-V-22D ML17292B3291998-04-0909 April 1998 LER 98-003-00:on 980311,WNP-2 Experienced SCRAM Signal as Result of Low Rpv.Caused by Less than post-SCRAM Operational Strategy for Resetting SCRAM Signal in Conditions.Changes in post-SCRAM Operational Strategy implemented.W/980409 Ltr ML17292B2661998-03-0404 March 1998 LER 98-001-00:on 980203,automatic Start of HPCS EDG Was Noted.Caused by Operator Error.Operations Crew Stabilized Plant at Approximately 75% Reactor Power & Investigation of Event Was initiated.W/980304 Ltr ML17292B1111997-11-10010 November 1997 LER 97-011-00:on 971010,HPCS Battery Charger Failed.Caused by Failure of a Phase Firing Control Circuit Board Due to Aging During 7 Yrs of Use.Hpcs Sys Was Immediately Declared inoperable.W/971110 Ltr ML17292B1151997-11-0707 November 1997 LER 97-010-00:on 970906,discovered That TS SR 3.4.5.1 for Identified Portion of RCS Total Leakage Would Not Be Able to Perform within Time Limits of SR 3.0.2.Caused by Inadequate Methods.Method of Meeting SR 3.4.5.1 Established ML17292B0641997-09-24024 September 1997 LER 97-004-01:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Indication of Entry Into Region a of power-to-flow Map.Caused by Inadequate Attention to Detail.Established Event Evaluation teams.W/970924 Ltr ML17292B0241997-08-18018 August 1997 LER 97-009-00:on 970717,discovered Error in Recently Performed Inservice Testing procedure,OSP-TIP/IST-R701. Caused by Procedure Inadequacy.Plant Procedure OSP/TIP/IST-R701 Will Be changed.W/970818 Ltr ML17292B0291997-08-15015 August 1997 LER 97-008-00:on 970716,wire Seal Used to Lock Containment Instrument Air Pressure Control valve,CIA-PCV-2B,found Not Intact.Cause of Misadjustment of CIA-PCV-2B Unknown.Event Will Be Communicated to Plant employees.W/970815 Ltr ML17292B0201997-08-15015 August 1997 LER 97-S01-00:on 970718,failure to Take Compensatory Measure for Inoperative Microwave Security Zone Occurred. Caused by Personnel Error.Training Will Be Conducted W/ Appropriate Members of Security force.W/970815 Ltr ML17292A9481997-07-23023 July 1997 LER 97-007-00:on 970611,voluntary Rept of Automatic Start of DG-1 & DG-2 Was Experienced.Caused by Undervoltage Condition on Electrical Busses SM-7 & SM-8.Circulating Water Pump CW-P-1C Control Switch Placed in pull-to-lock.W/970723 Ltr ML17292A9201997-06-26026 June 1997 LER 97-006-00:on 970527,non-performance of Surveillance Requirement 3.6.1.3.2 for Blind Fanges,Was Noted.Caused Because Misunderstanding of Intent of Specs.Added Five Structural Assemblies for SP.W/970626 Ltr ML17292A8331997-04-28028 April 1997 LER 97-004-00:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Entry Into Region a of power-to-flow Map Following Planned Trip of Single Mfp. Event Evaluation teams,established.W/970428 Ltr ML17292A8311997-04-28028 April 1997 LER 97-005-00:on 970327,valid Reactor Scram Signal Received Due to Low Water Level Condition During Preparations for SRV Testing.Caused by Risks & Consequences of Decisions Not Completely Identified.Restored Water level.W/970428 Ltr ML17292A8251997-04-21021 April 1997 LER 97-003-00:on 970320,notification of Noncompliance W/Ts as TS SRs for Response Time Testing Were Not Being Met for Specified Instrumentation in Rps,Pcis & Eccs.Requested Enforcement Discretion for One Time exemption.W/970421 Ltr ML17292A7431997-03-20020 March 1997 LER 97-002-00:on 970218,determined That Rod Block Monitor (RBM) Calibr Values Were Not Set IAW Tech Specs.Caused by Calibr Procedures Inadequacies.Revised & re-performed RBM Channel Calibr procedures.W/970330 Ltr ML17292A7401997-03-13013 March 1997 LER 97-001-00:on 970211,reactor Water Cleanup Sys Blowdown Flow Isolation Setpoint Was Slightly Above TS Allowable Valve Occurred Due to Calculation Error.Lds Fss LD-FS-15 LD-FS-16 Were Declared inoperable.W/970313 Ltr ML17292A6641997-01-22022 January 1997 LER 96-009-00:on 961220,miscalculation of Instantaneous Overcurrent Relay Settings Resulted in Inoperability of safety-related Equipment.Caused by Utilization of Inappropriate Design.Testing Was completed.W/970122 Ltr ML17292A6461997-01-0606 January 1997 LER 96-008-00:on 961205,failure to Comply with TS Action Requirement for Emergency Core Cooling Sys Actuation Instrumentation Occurred Due to Unidentified Inoperability Condition.Pmr initiated.W/970106 Ltr ML17292A6371996-12-19019 December 1996 LER 96-007-00:on 961122,electrical Breakers Were Not Seismically Qualified in Test/Disconnect Position.Circuit Breaker Mfg Did Not Consider Raced Out Breaker Position During Testing.Relocated Circuit breakers.W/961217 Ltr ML17292A4121996-08-0808 August 1996 LER 96-006-00:on 960709,average Power Range Monitor Rod Block Downscale Surveillance Not Performed Prior to Entry Into Mode 1.Caused by long-standing Misinterpretation of Requirements of Tss.Procedures revised.W/960808 Ltr ML17292A3801996-07-24024 July 1996 LER 96-004-00:on 960624,plant Was Manually Scrammed by Control Room Personnel Due to Reactor Water Level Transient Experienced During Testing of Digital Feedwater Sys.Caused by Programming Error.Sys Was corrected.W/960724 Ltr ML17292A3771996-07-24024 July 1996 LER 96-005-00:on 960624,determined Missed Surveillance Test Re Channel Check of Average Power Range Monitor.Caused by Inadequate Procedures.Revised Surveillance Procedure Re When APRM Checks Must Be performed.W/960724 Ltr ML17292A3641996-07-12012 July 1996 LER 96-003-00:on 960615,required Surveillance Test Not Performed When Required by TS 3.4.1.3.Caused by Inadequate Procedures.Implementing Surveillance Procedure & Reactor Plant Startup Procedures revised.W/960712 Ltr ML17292A3361996-06-20020 June 1996 LER 96-002-00:on 960504,critical Bus SM-8 Lost Power When Supply Breaker 3-8 Tripped.Caused by Personnel Error. Operators Counselled & Procedures revised.W/960620 Ltr ML17292A2861996-05-24024 May 1996 LER 96-001-00:on 960425,inadvertent ESF Actuations Occurred Due to Tripping of Temporary Power Supply to IN-3.Caused by Personnel Error.Operations Restored to IN-3 Loads & Reset ESF actuations.W/960524 Ltr ML17291B0891995-10-19019 October 1995 LER 95-011-00:on 950919,failed to Comply W/Ts SR for RCIC Sys Due to Analysis Deficiency That Resulted in Inadequate Surveillance Test Procedure.Surveillance Procedure Revised to Correct deficiency.W/951019 Ltr ML17291A9021995-07-0707 July 1995 LER 95-010-00:on 950609,HPCS DG Declared Inoperable Due to Discovery That TS Test Method Incomplete.Caused by Inadequate Testing Procedure.Test Procedure for HPCS DG Reviewed & Special Test Procedures written.W/950707 Ltr ML17291A9031995-07-0707 July 1995 LER 95-009-00:on 950607,inadvertent MSIV Closure Occurred During Surveillance Test Due to Poor Communication Between Test Team.Determined That MSIV Closure Not Valid Because Closure Not Triggered by Plant conditions.W/950707 Ltr ML17291A8501995-06-0808 June 1995 LER 95-006-01:on 950405,reactor Scram Occurred During Surveillance Testing Due to Protective Sys Relay Failure. Replaced Failed Relay Before Plant Startup ML17291A8101995-05-12012 May 1995 LER 95-008-00:on 940125,TS Wording Lead to Potential TS Violation.Caused by Lack of Clarity in Ts.Submitted Improved TS for Plant to Provide Addl clarity.W/950512 Ltr ML17291A7841995-05-0505 May 1995 LER 95-007-00:on 950222,emergency Diesel Start Occurred Due to Voltage Transient on BPA Grid.Confirmation Was Received at 17:51 H That Disturbance Had Originated in BPA Grid ML17291A7801995-05-0404 May 1995 LER 95-006-00:on 950405,main Turbine Trip Occurred During Performance of Surveillance Test Due to Protective Sys Relay Failed.Replaced Failed Relay Before Plant startup.W/950504 Ltr ML17291A7851995-05-0303 May 1995 LER 95-005-00:on 950222,inoperable IRM Had Been Relied Upon to Meet TS Requirements During Reactor Startup.Caused by Lack of Neutron Source to Test Instrumentation. Sys Knowledge Gained Will Be incorporated.W/950503 Ltr ML17291A7071995-03-25025 March 1995 LER 95-004-00:on 950226,malfunction in Main Turbine DEH Control Sys Caused All Four High Pressure Turbine Governor Valves to Rapidly Close.Caused by Blown Fuse.Suspected Faulty Circuit Card replaced.W/950325 Ltr ML17291A7011995-03-20020 March 1995 LER 95-002-00:on 950218,automatic Reactor Scram Occurred. Caused by Erroneous Positioning of Control During Performance of Scheduled Periodic Functional Test.Control repositioned.W/950320 Ltr 1999-07-20
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17284A9001999-10-31031 October 1999 Rev 0 to COLR 99-15, WNP-2 Cycle 15,COLR GO2-99-177, LER 99-S01-00:on 990903,failure to Take Compensatory Measure within Required Time Upon Failure of Isolation Zone Microwave Unit,Was Noted.Caused by Personnel Error.Provided Refresher Training on Compensatory Measures.With1999-10-0101 October 1999 LER 99-S01-00:on 990903,failure to Take Compensatory Measure within Required Time Upon Failure of Isolation Zone Microwave Unit,Was Noted.Caused by Personnel Error.Provided Refresher Training on Compensatory Measures.With ML17284A8941999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for WNP-2.With 991012 Ltr ML17284A8801999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for WNP-2.With 990910 Ltr ML17284A8691999-07-31031 July 1999 Monthly Operating Rept for July 1999 for WNP-2.With 990813 Ltr ML17292B7421999-07-20020 July 1999 LER 99-001-00:on 990628,ESF Signal Closed All Eight MSIVs While Plant Was Shutdown.Caused by Failure of Relay RPS-RLY-K10D.Subject Relay Was Replaced & Tested on 990630. with 990720 Ltr ML17292B7271999-06-30030 June 1999 Monthly Operating Rept for June 1999 for WNP-2.With 990707 Ltr ML17292B6961999-05-31031 May 1999 Monthly Operating Repts for May 1999 for WNP-2.With 990608 Ltr ML17292B6641999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for WNP-2.With 990507 Ltr ML17292B6391999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for WNP-2.With 990413 Ltr ML17292B5871999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for WNP-2.With 990311 Ltr ML17292B5571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for WNP-2.With 990210 Ltr ML17292B5621999-01-31031 January 1999 Rev 1 to COLR 98-14, WNP-2 Cycle 14 Colr. ML17292B5341999-01-15015 January 1999 Part 21 Rept Re Incorrect Modeling of BWR Lower Plenum Vol in Bison.Defect Applies Only to Reload Fuel Assemblies Currently in Operation at WNP-2.BISON Code Model for WNP-2 Has Been Revised to Correct Error ML17292B5331999-01-15015 January 1999 Part 21 Rept Re XL-S96 CPR Correlation for SVEA-96 Fuel. Defect Applies Only to WNP-2,during Cycles 12,13 & 14 Operation.Evaluations of Defect Performed by ABB-CE ML17292B4791998-12-31031 December 1998 Washington Public Power Supply Sys 1998 Annual Rept. with 981215 Ltr ML17292B5351998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for WNP-2.With 990112 Ltr ML17292B5741998-12-31031 December 1998 WNP-2 1998 Annual Operating Rept. with 990225 Ltr ML17284A8231998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for WNP-2.With 981207 Ltr ML17284A8081998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for WNP-2.With 981110 Ltr ML17292B4451998-10-27027 October 1998 LER 98-012-01:on 980715,failure to Comply with Requirements of TS SR 3.8.4.7 Was Noted.Caused by Inadequate Work Practices.Training Session Was Held with Personnel.With 981027 Ltr ML17284A7831998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for WNP-2.With 981007 Ltr ML17284A7491998-09-10010 September 1998 WNP-2 Inservice Insp Summary Rept for Refueling Outage RF13 Spring,1998. ML17284A7561998-09-0303 September 1998 LER 98-013-00:on 980805,ESF Actuations Were Noted Due to Deenergization of Vital Electrical Bus SM-8.Caused by Inadequate Direction in Troubleshooting Plan.Will Conduct Training for Engineering Personnel.With 980903 Ltr ML17284A7571998-09-0202 September 1998 LER 98-014-00:on 980807,completion of TS 3.8.1.F Required Shutdown Due to Inoperability of EDG-2 Was Noted.Caused by Degraded Voltage Regulator for DG-2.Replaced Voltage Regulator & Associated Scrs.With 980902 Ltr ML17284A7551998-09-0202 September 1998 LER 98-015-00:on 980808,discovered Reactor Coolant Pressure Boundary Leak During Shutdown Conditions.Caused by Leakage from Socket Weld (Fwb 63) on Elbow Connection.Failed Piping Connection Was Replaced.With 980902 Ltr ML17284A7681998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for WNP-2.With 980915 Ltr ML17284A7311998-08-17017 August 1998 LER 98-012-00:on 980716,determined That 24-month SR 3.8.4.7 Had Not Been Fulfilled within Specified Frequency.Caused by Inadequate Work Practices.License Requested & Received Enforcement Discretion Re Battery Svc test.W/980817 Ltr ML17284A7261998-07-31031 July 1998 Monthly Operating Rept for July 1998 for WNP-2.W/980810 Ltr ML17284A7121998-07-23023 July 1998 LER 98-006-01:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of 10CFR50,App R Calculations for High Impedance Faults.Caused by Inadequate Work Practices.Implemented Procedural Changes ML17284A6951998-07-17017 July 1998 LER 98-011-00:on 980617,ECCS Pump Room Flooding Was Noted Due to FP Sys Pipe Break.Caused by Inadequate Design of FP Sys.Detailed Review of FP Sys Design Was Conducted. W/980717 Ltr ML17284A6961998-07-15015 July 1998 LER 98-010-00:on 980615,TS Required Shutdown Due to Inoperability of TIP Sys Isolation Valve Was Noted.Caused by Improper Installation of TIP Tubing.Reattached Affected Tubing & Inspected Other TIP tubing.W/980715 Ltr ML17284A6731998-07-0101 July 1998 LER 98-009-00:on 980606,nuclear Steam Supply Shutoff Sys Group 3 & 4 Isolations During Testing Was Noted.Caused by Procedural Deficiency.Counseled Individuals Involved in preparation.W/980701 Ltr ML17284A6751998-06-30030 June 1998 Ro:On 980617,flooding of RB Northeast Stairwell with Consequential Flooding of Two ECCS Pump Rooms.Caused by Inadequate Fire Protection Sys Design.Pumped Out Water from Affected Areas to Point Below Berm Areas of Pump Rooms ML17284A6641998-06-24024 June 1998 LER 98-008-00:on 980531,inadvertent Full Scram During RPV Leak Testing in Mode 4 Was Noted.Caused by Change in Mgt Techniques.Revised Procedures to Take Into Account Addl Water Head in Pressure Sensing lines.W/980624 Ltr ML17284A6651998-06-24024 June 1998 LER 98-007-00:on 980530,inadvertent Full Scram & Division 1 ECCS Injection Was Noted.Caused by Failure to Meet Mgt Work Practice Expectation When Encountering Deficient Procedure. Incident Review Board Convened to Review event.W/980624 Ltr ML17284A6631998-06-19019 June 1998 LER 98-006-00:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of App R Calculations for High Impedance Fault Analysis.Caused Indeterminate. Implemented Procedural Changes Involving Operator Action ML17284A6551998-06-0404 June 1998 LER 98-005-00:on 980506,potential for Failure of RHR Sys Valve to Close on Isolation Signal Was Noted.Caused by Design Deficiency.Caution Tag Was Placed on RHR-V-40 Control Switch to Inform Plant Operators of limitation.W/980604 Ltr ML17284A6421998-06-0101 June 1998 LER 98-004-00:on 980502,determined That Primary Containment Penetration Overcurrent Protection Does Not Meet Reg Guide 1.63 Requirements.Caused by Inadequate Design Changes. Installed Addl Fuse in RHR-MO-9 circuit.W/980601 Ltr ML17284A6491998-05-31031 May 1998 Rev 0 to COLR 98-14, WNP-2,Cycle 14 Colr. ML17292B4031998-05-31031 May 1998 Monthly Operating Rept for May 1998 for WNP-2.W/980608 Ltr ML17292B3921998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for WNP-2.W/980513 Ltr ML17292B3291998-04-0909 April 1998 LER 98-003-00:on 980311,WNP-2 Experienced SCRAM Signal as Result of Low Rpv.Caused by Less than post-SCRAM Operational Strategy for Resetting SCRAM Signal in Conditions.Changes in post-SCRAM Operational Strategy implemented.W/980409 Ltr ML17292B3281998-04-0909 April 1998 LER 98-002-00:on 980311,reactor Scram & Plant Transient Occurred,Due to Failed Closed Main Steam Isolation Valve. Caused by Loss of Pneumatic Actuating Supply Pressure. Problem Evaluation Request Written for Failure of MS-V-22D ML17292B3371998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for WNP-2.W/980409 Ltr ML17292B2641998-03-0404 March 1998 Performance Self Assessment,WNP-2. ML17292B2661998-03-0404 March 1998 LER 98-001-00:on 980203,automatic Start of HPCS EDG Was Noted.Caused by Operator Error.Operations Crew Stabilized Plant at Approximately 75% Reactor Power & Investigation of Event Was initiated.W/980304 Ltr ML17292B2911998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for WNP-2.W/980313 Ltr ML17284A7971998-02-17017 February 1998 Rev 28 to Operational QA Program Description, WPPSS-QA-004.With Proposed Rev 29 ML17292B3591998-02-12012 February 1998 WNP-2 Cycle 14 Reload Design Rept. 1999-09-30
[Table view] |
Text
ACCEI ERATO DOCUMENT DIST UTION SYSTEM REGULATORY INFORMATION DISTRIBUTION STEM (RIDS)
]'/ACCESSION NHR:9303100200 DOC.DATE: 93/03/04 NOTARIZED: NO DOCKET FACIL:50-397 WPPSS Nuclear Project, Unit 2, Washington Public Powe 05000397 AUTH. NAME AUTHOR AFFILIATION POCHE,P.J. Washington Public Power Supply System BAKER,J.W. Washington Public Power Supply System RECIP.NAME RECIPIENT AFFILIATION
SUBJECT:
LER 93-005-00:on 930202,inadequate documentation 6 review of operability status results in unavailability of wetwell purge exhaust valve. Caused by technical inadequacies.Wetwell valves adjusted 6 returned to operable status.W/930304 ltr.
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
U SIZE'ITLE:
NOTES:
RECIPIENT COPIES'TTR RECIPIENT COPIES ID CODE/NAME ENCL ID CODE/NAME LTTR ENCL PD5 LA 1 1 PD5 PD 1 1 CLIFFORDgJ 1 1 INTERNAL: ACNW 2 2 ACRS 2 2 AEOD/DOA 1 1 AEOD/DSP/TPAB 1 1 AEOD/ROAB/DSP 2 2 NRR/DE/EELB 1 1 NRR/DE/EMEB 1 1 NRR/DORS/OEAB 1 1 NRR/DRCH/HHFBHE 1 1 NRR/DRCH/HICB 1 1 NRR/DRCH/HOLB 1 1 NRR/DRIL/RPEB 1 1 NRR/DRSS/PRPB 2 2 NRR/DSSA/SPLB 1 1 NRR/DSSA/SRXB 1 1 ~REG~F~E 02 1 1 RES/DSIR/EIB 1 1 RGN5 FILE 01 1 1 EXTERNAL: EGG(G BRYCE,J.H 2 2 L ST LOBBY WARD 1, 1 NRC PDR 1 1 NSIC MURPHYgG.A 1 1 NSIC POOREiW 1 1 NUDOCS FULL TXT 1 1 NOTE TO ALL"RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTETH CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT. 504-2065) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 32 ENCL 32
ti WASHINGTON PUBLIC POWER SUPPLY SYSTEM P.O. Box 968 ~ 3000 George Washington Way ~ Richland, Washington 99362 March 4, 1993 G02-93-053 Docket No. 50-397 Document Control Desk U.S. Nuclear Regulatory Commission Washington, D.C. 20555
SUBJECT:
NUCLEAR PLANT WNP-2, OPERATING LICENSE NPF-21 LICENSEE EVENT REPORT NO.93-005 Transmitted herewith is Licensee Event Report No.93-005 for the WNP-2 Plant. This report is submitted in response to the report requirements of 10CFR50.73 and discusses the items of reportability, corrective action taken, and action taken to preclude recurrence.
Sincerely, J. W. Baker WNP-2 Plant Manager (Mail Drop 927M)
JWB/RJP/my Enclosure CC: Mr. J. B. Martin, NRC - Region V Mr. R. Barr, NRC Resident Inspector (Mail Drop 901A, 2 Copies)
INPO Records Center - Atlanta, GA Mr. D. L. Williams, BPA (Mail Drop 399) 09013.0 9303i00200 930304 PDR ADOCK 05000397 8 PDR
LICENSEE EVEN EPORT (LER)
AGILITY HAHE (1) DOCKET NUMB R ( ) PAGE (3)
Washin ton Nuclear Plant - Unit 2 0 5 0 0 0 3 9 7 I OF ITLE (4)
INADEQUATEDOCUMENTATION AND REVIEW OF OPERABILITY STATUS RESULTS IN UNAVAILABILITY OF WETWELL PURGE EXHAUST VALVEDURING REQUIRED CONDITIONS EVENT DATE (5 LER HUHBER 6 REPORT DATE (7 OTHER FACILITIES INVOLVED (8)
MONTH DAY YEAR SEQUENTIAL ",:c EV ISIOH MONTM OAY YEAR FACILITY NAMES CKE NUMB R (5)
NUMBER C? UMBER 0 0 0 0 2 0 2 9 3 9 3 0 0 5 0 0 0 3 0 4 9 3 000 PERATING MIS REPORT IS SUBMITTED PURSUAHT To THE REQUIREMENTS OF 10 CFR 5: (Check one or more of the following) (ll ODE (9) 3 O'NER LEVEL 0.402(b) 20.405(C) 50.73(a)(2)(iv) 77.71(b)
(10) O.4OS(a)(1)(i) 50.36(c)(1) 50.73(a)(2)(v) 73.73(c)
O.4OS(a)(1)( <<) 50.36(c)(2) 50.73(a)(2)(vii) THER (Specify in Abstract O.4OS(a)(1)(iii) X 0.73(a)(2)(i) 50.73(a)(2)(viii)(A) elow and in Text, NRC 0.405(a)(1)(iv) 50.73(a)(2)(ii) 50.73(a)(2)(viii)(B) orm 366A) 0.405(a)(1)(v) 50.73(a)(2)(iii) 50.73(a)(2)(x)
LICENSEE CONTACT FOR THIS LER 12 TELEPMONE NUMBER REA CODE R. Z. Pochh, Licensing Engineer 0 9 7 7 - 4 1 4 5 COHPLETE ONE LINE FOR EACH COHPONEHT FAILURE OESCRIBEO IN THIS REPORT (13)
CAUSE SYSTEH COHPOHENT HANUFACTURER EPORTABLE:;:7?Tc">. CAUSE SYSTEM COHPOHEHT HANUFACTURER REPORTABLE 0 NPRDS Ng~~ TO NPRDS 4?F<.(4@
SUPPLEMENTAL REPORT EXPECTED (14) EXPECTED SUBHISSION MONTH OAY YEAR ATE (15)
YES (If yes, carplete EXPECTED SUBHISSIOH DATE) X HO TRACT OO At 1557 hours0.018 days <br />0.433 hours <br />0.00257 weeks <br />5.924385e-4 months <br /> on February 2, 1993, it was identified that the plant had entered into an Operational Condition where the Wetwell Purge Exhaust Valves were required to be operable without performing Technical Specification required maintenance. Technical Specification Surveillance Requirement 4.6.1.8.2.b specifies that these valves are to be secured closed, and maintenance performed during the next plant cold shutdown if their leakrate is greater than 0.05 La. The valves were secured shut after their leakrate was measured to be greater than 0.05 La on November 23, 1992. However, the plant entered Operational Condition 4 (cold shutdown) on January 21, 1993, and was later restarted on January 28, 1993 without performing valve maintenance.
This event had two root causes. The primary cause was technical inaccuracies in documents written to document the failed LLRT on November 23, 1992. The secondary cause was required verifications that were not adequately performed. As corrective actions, the affected valve was repaired, procedures regarding preparation, review and use of LCO/INOP Status Sheets will be revised, required reading will be provided, and expectations regarding review of deficient conditions involving Technical Specification required equipment and systems will be communicated to Control Room Supervisors and Shift Managers.
WNP-2 did not experience an event that required use of the affected valves during the period when their leakrate exceeded limits. Consequently, this condition did not have an adverse affect on safe operation of the plant, or the health and safety of plant personnel or the general public.
LICENSEE EVENT REPORT (L )
TEXT CONTINUATION AGILITY NAHE (i) OOCKET NUHBER (2) LER NUHBER (8) AGE (3) ear umber ev. No.
Washington Nuclear Plant - Unit 2 0 5 0 0 0 3 9 7 3 005 00 2 F 7 iTLE (4)
INADEQUATE DOCUMENTATION AND REVIEW OF OPERABILITY STATUS RESULTS IN UNAVAILABILITYOF WETWELL PURGE EXHAUST VALVE DURING REQUIRED CONDITIONS Pl n ndii n Plant Mode - 3 (Hot Shutdown)
Power Level - 0%
Evn D ri in At 1557 hours0.018 days <br />0.433 hours <br />0.00257 weeks <br />5.924385e-4 months <br /> on February 2, 1993, a plant engineer identified that the plant had entered into an Operational Condition where the Wetwell Purge Exhaust Valves (CEP-V-3A, CEP-V-4A) were required to be operable without performing maintenance necessary to satisfy Technical Specification Surveillance Requirement 4.6.1.8.2.b. This Surveillance Requirement specifies that the Wetwell Purge Exhaust Valves are to be secured closed, and corrective maintenance performed during the next plant cold shutdown if their leakrate is greater than 0.05 La. The Wetwell Purge Exhaust Valves had been secured shut on November 23, 1992 after their leakrate was measured to be greater than 0.05 La. However, the plant entered Operational Condition 4 (cold shutdown) on January 21, 1993, and was later restarted on January 28, 1993 without performing the required maintenance.
Immedia e rr 've Action As immediate corrective action, the applicable Technical Specification Limiting Conditions for Operation (LCOs) were entered, and efforts were initiated to return the Wetwell Purge Exhaust Valves to operable status.
her Eval i n R n rr iveA i n A. ~h The condition described in this report is reportable pursuant to the requirements of 10CFR50.73(a)(2)(i)(B) as an operation or condition that is prohibited by the plant Technical Specifications. Corrective maintenance required by Technical Specification Surveillance Requirement 4.6.1.8.2.b was not performed prior to restarting the plant from Operational Condition 4.
- 2. On November 23, 1992, an LLRT was performed on valves CEP-V-3A and CEP-V-4A.
The measured leakrate for these valves was in excess of the 0.05 La leakrate limit imposed by Technical Specification Surveillance Requirement 4.6.1.8.2.a. Consequently, in accordance with Technical Specification Surveillance Requirement 4.6.1.8.2.b, the valves were secured closed. Additionally, the Shift Manager initiated a Problem Evaluation Request (PER) to document this condition, and an LCO/INOP Status Sheet was prepared to track inoperability of the valves.
LICENSEE EVENT REPORT (L R)
TEXT CONTINUATION ACILITY NANE (1) OOCKET NUHBER (2) LER NUMBER (8) AGE (3) ear umber ev. No.
Washington Nuclear Plant - Unit 2 0 5 0 0 0 3 9 7 3 005 00 3 F 7 ITLE (4)
INADEQUATE DOCUMENTATION AND REVIEW OF OPERABILITY STATUS RESULTS IN UNAVAILABILITYOF WETWELL PURGE EXHAUST VALVE DURING REQUIRED CONDITIONS The LCO/INOP Status Sheet that was initiated correctly reflected Technical Specification Requirements to secure the valves closed and perform an LLRT if the valves were operated.
However, it did not correctly document the Technical Specification required Action that is contained within Surveillance Requirement 4.6.1.8.2.b. This action requires performance of corrective maintenance prior to restart from the next plant cold shutdown. Additionally, the PER that was written to document the failed LLRT did not reference the cold shutdown requirement, and incorrectly suggested that it would be acceptable to perform the repair work prior to restart from the next refueling outage.
Inoperability of the Wetwell Purge Exhaust Valves was discussed on the morning of November 24, 1992 during the Work Control Daily Plant Status meeting, and the valves were added to the LCOs/Compensatory Measures list. During this meeting, a maintenance work request (MWR) was identified that had been previously written to replace seals on the Wetwell Purge Exhaust Valves. It was not recognized that the priority assigned to this MWR, which was scheduled for performance during the next refueling outage, would not be adequate to satisfy Technical Specification requirements if the plant entered Operational Condition 4 prior to the refueling outage.
'he PER written to document Wetwell Purge Exhaust Valve inoperability was also discussed on the morning of November 24 during a Management Review Committee (MRC) meeting.
This discussion was largely influenced by inaccurate information provided on the PER, and also by the discussion that was held earlier that morning in the Work Control Daily Plant Status meeting. The PER review performed by MRC was conducted in an overview capacity, and was not intended to supercede the primary plant processes used to identify conditions that can affect plant operations. However, this review was an opportunity to recognize that the PER, which suggested that repair activities could be performed during the next refueling outage, might not be adequate to satisfy Technical Specification requirements.
- 3. An automatic scram was experienced at 0944 hours0.0109 days <br />0.262 hours <br />0.00156 weeks <br />3.59192e-4 months <br /> on January 21, 1993 following an unplanned main feedwater pump trip. The plant reached Operational Condition 4 at 2057 hours0.0238 days <br />0.571 hours <br />0.0034 weeks <br />7.826885e-4 months <br /> the same day. In preparation for restart, the Minimum Startup Checklist was completed at 1430 hours0.0166 days <br />0.397 hours <br />0.00236 weeks <br />5.44115e-4 months <br /> on January 28, 1993. This checklist includes a review of LCO/INOP Log Sheets. When this review was performed it did not identify repair of CEP-V-3A and CEP-V-4A as a constraint to restart.
LlCENSEE EVENT REPORT (L )
TEXT CONTINUATION
'CILlTT NAHE (i) 00CKET NUHBER (2) LER NUHBER (8) AGE (3) ear umber ev. No.
Washington Nuclear Plant - Unit 2 p 8 P P P 3 9 7 3 005 0 4 F 7 ITLE (4)
INADEQUATE DOCUMENTATION AND REVIEW OF OPERABILITY STATUS RESULTS IN UNAVAILABILITYOF WETWELL PURGE EXHAUST VALVE DURING REQUIRED CONDITIONS The Wetwell Purge Exhaust Valves are required in Operational Conditions 1 through 3.
Following the January 21, 1993 shut down, the plant first entered into an Operational Condition where the valves were required to be operable at 1734 hours0.0201 days <br />0.482 hours <br />0.00287 weeks <br />6.59787e-4 months <br /> on January 28, 1993.
The plant was subsequently operated between Operational Conditions 1 and 3 until February 3, 1993. During this time a low oil level alarm was received for one of the reactor recirculation (RRC) pumps.
In order to investigate the cause of this alarm, actions were taken on the morning of February 2, 1993 to deinert primary containment so that a drywell entry could be made.
Deinerting primary containment requires operation of the Wetwell Purge Exhaust Valves, and in accordance with Technical Specifications, an LLRT must be performed if these valves are operated. Consequently, following completion of the purge evolution, an LLRT was performed on the afternoon of February 2, 1993. The results of this LLRT demonstrated a leakrate in excess of Technical Specification limits.
The applicable Limiting Conditions for Operation (LCOs) were entered for Technical Specifications 4.6.1.8.2.b and 3.6.1.1 at 1558 hours0.018 days <br />0.433 hours <br />0.00258 weeks <br />5.92819e-4 months <br /> on February 2, 1993. It was also during this same approximate time frame when the system engineer identified that the plant had previously operated in Operational Conditions where the Wetwell Purge Exhaust Valves were required while the valves were in an inoperable condition.
Efforts to reduce valve leakage by performing linkage adjustments were unsuccessful. As a result, it became necessary to enter Operational Condition 4 so that the spool piece installed between CEP-V-3A and CEP-V-4A could be removed and repairs made. This evolution did not constitute a Technical Specification required plant shut down because the plant was already in Operational Condition 3 (hot shutdown) when the failure to perform required maintenance was identified. The plant reached Operational Condition 4 at 0925 hours0.0107 days <br />0.257 hours <br />0.00153 weeks <br />3.519625e-4 months <br /> on February 3, 1993 (approximately 17.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> after discovery).
Testing of CEP-V-3A and CEP-V-4A determined that the leakrate for the outboard valve was acceptable (less than 0.05 La), and that the excess leakage was through the inboard isolation valve. Physical examination of the seal for the inboard valve did not identify damage.
Adjustment nuts on the retaining ring for the soft seal of the inboard valve were each tightened in order to expand the seal material, and the valve was subsequently leakrate tested and found to be acceptable. Both valves were returned to operable status at 1747 hours0.0202 days <br />0.485 hours <br />0.00289 weeks <br />6.647335e-4 months <br /> on February 4, 1993.
LICENSEE EVENT REPORT (L R)
TEXT CONTINUATION AGILITY HAHE (1) OOCKET HUHBER (2) LER HUHBER (B) AGE (3) ear umber ev. Ho.
Washington Nuclear Plant - Unit 2 0 5 0 0 0 3 9 7 3 005 0 5 F 7 ITLE (4)
INADEQUATE DOCUMENTATION AND REVIEW OF OPERABILITY STATUS RESULTS IN UNAVAILABILITYOF WETWELL PURGE EXHAUST VALVE DURING REQUIRED CONDITIONS B. Ro~gge There were two root causes for the condition described in this report. The primary root cause involved failure to fully and/or correctly document the maintenance requirement described within Technical Specification Surveillance Requirement 4.6.1.8.2.b on either the LCO/INOP Status Sheet or the PER. This cause involved Written Procedures and Documents category deficiencies within the Technical Inaccuracies subcategory.
The secondary root cause involved three instances whereby the Technical Specification required Action to perform valve maintenance was not identified. These examples involved Personnel-Work Practices category deficiencies that resulted from Required Verifications that were not Adequately Performed. The first two examples involved errors by licensed, utility personnel, and the third example involved an error by non-licensed, utility personnel.
The first example resulted when requirements to repair CEP-V-3A and CEP-V-4A were not recognized to be a constraint for restart from Operational Condition 4 during performance of the Minimum Startup Checklist. As directed in procedures, the review of LCO/INOP Status Sheets that is associated with this checklist should have identified this constraint.
- 2. The second example resulted when maintenance activities necessary to return the Wetwell Purge Exhaust Valves to operable status were not recognized to be a constraint to restart from Operational Condition 4 by personnel in Work Planning. In accordance with plant procedures, it is the responsibility of the Operations Work Control Coordinator to ensure that work control activities are adequately identified and scheduled to maintain compliance with the plant Technical Specifications.
- 3. The third example involved failure to recognize that repair of CEP-V-3A and CEP-V-4A was a constraint for restart from Operational Condition 4 during MRC review of the PER. This review did not fully satisfy requirements established in plant procedures.
LICENSEE EVENT REPORT (L R)
TEXT CONTINUATION AGILITY NAHE (1) DOCKET NUHBER (2) LER NUHBER (8) AGE (3) ear umber ev. No.
Washington Nuclear Plant - Unit 2 0 5 0 0 0 3 9 7 3 005 0 6 F 7 ITLE (4)
INADEQUATE DOCUMENTATION AND REVIEW OF OPERABILITY STATUS RESULTS IN UNAVAILABILITYOF WETWELL PURGE EXHAUST VALVE DURING REQUIRED CONDITIONS C. F r rr i A i n The following corrective actions either have been, or will be taken:
The Wetwell Purge Exhaust Valves, CEP-V-3A and CEP-V-4A, were adjusted and returned to operable status.
- 2. The PER process has recently undergone a major upgrade and revision. The revised process incorporates provisions that have provided overall stengthening of the PER process, and includes specific improvements that address the review of deficient conditions for restart impact.
- 3. Procedure PPM 1.3.1D, Conduct of Operations, will be revised to provide more detailed direction regarding information that should be provided on LCO/INOP Status Sheets. Also, the revised procedure and a copy of this LER will be placed in required reading for licensed Operations personnel. Completion of the procedure change and required reading distribution is scheduled for March 15, 1993.
- 4. Management expectations with regard to review of deficient conditions involving Technical Specification required equipment and systems will be communicated to Control Room Supervisors and Shift Managers. Completion of this action is scheduled for March 5, 1993.
Safet i nifican WNP-2 did not experience an event that required use of the safety function associated with the Wetwell Purge Exhaust Valves during the period when the measured leakrate was in excess of Technical Specification limits. Consequently, the condition described in this report did not have an adverse affect on safe operation of the plant, or the health and safety of plant personnel or the general public. Additionally, although the leakrate associated with the Wetwell Purge Exhaust penetration was in excess of Technical Specification limits, the excess leakage was limited to the inboard valve. As a result, even if an event had occurred, plant operation within the release limits of 10CFR100 would have been assured.
imil r Ev n An event involving leakrate testing of the drywell airlock was reported in LER 91-028. This event involved testing that was initiated, but not completed, within the allowed interval due to inadequate tracking of an LCO action. Additionally, previous events involving Technical Specification directed actions that were not met due to inadequate tracking of LCO actions have been reported in LERs92-038 and 92-046.
These previous events involved actions that were tracked under the Chemistry LCO Log, and did not involve the Operations LCO/INOP Log.
LICENSEE EVENT REPORT (L )
TEXT CONTINUATION AGILITY NAME (I) DOCKET NUMBER (2) LER NUMBER (8) AGE (3) ear umber ev. No.
Washington Nuclear Plant - Unit 2 P
0 5 0 0 0 3 9 7 3 05 0 7 F 7 ITLE (4)
INADEQUATE DOCUMENTATION AND REVIEW OF OPERABILITY STATUS RESULTS IN UNAVAILABILITYOF WETWELL PURGE EXHAUST VALVE DURING REQUIRED CONDITIONS EII Inf rm tion Tx Rfr R f
/~<emm~om o~nen Wetwell Purge Exhaust Valves, CEP-V-3A & VB PDCV CEP-V-4A Reactor Recirculation Pumps AD Primary Containment, Wetwell NH Standby Gas Treatment System BH