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Category:LICENSEE EVENT REPORT (SEE ALSO AO
MONTHYEARML17292B7421999-07-20020 July 1999 LER 99-001-00:on 990628,ESF Signal Closed All Eight MSIVs While Plant Was Shutdown.Caused by Failure of Relay RPS-RLY-K10D.Subject Relay Was Replaced & Tested on 990630. with 990720 Ltr ML17292B4451998-10-27027 October 1998 LER 98-012-01:on 980715,failure to Comply with Requirements of TS SR 3.8.4.7 Was Noted.Caused by Inadequate Work Practices.Training Session Was Held with Personnel.With 981027 Ltr ML17284A7561998-09-0303 September 1998 LER 98-013-00:on 980805,ESF Actuations Were Noted Due to Deenergization of Vital Electrical Bus SM-8.Caused by Inadequate Direction in Troubleshooting Plan.Will Conduct Training for Engineering Personnel.With 980903 Ltr ML17284A7571998-09-0202 September 1998 LER 98-014-00:on 980807,completion of TS 3.8.1.F Required Shutdown Due to Inoperability of EDG-2 Was Noted.Caused by Degraded Voltage Regulator for DG-2.Replaced Voltage Regulator & Associated Scrs.With 980902 Ltr ML17284A7551998-09-0202 September 1998 LER 98-015-00:on 980808,discovered Reactor Coolant Pressure Boundary Leak During Shutdown Conditions.Caused by Leakage from Socket Weld (Fwb 63) on Elbow Connection.Failed Piping Connection Was Replaced.With 980902 Ltr ML17284A7311998-08-17017 August 1998 LER 98-012-00:on 980716,determined That 24-month SR 3.8.4.7 Had Not Been Fulfilled within Specified Frequency.Caused by Inadequate Work Practices.License Requested & Received Enforcement Discretion Re Battery Svc test.W/980817 Ltr ML17284A7121998-07-23023 July 1998 LER 98-006-01:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of 10CFR50,App R Calculations for High Impedance Faults.Caused by Inadequate Work Practices.Implemented Procedural Changes ML17284A6951998-07-17017 July 1998 LER 98-011-00:on 980617,ECCS Pump Room Flooding Was Noted Due to FP Sys Pipe Break.Caused by Inadequate Design of FP Sys.Detailed Review of FP Sys Design Was Conducted. W/980717 Ltr ML17284A6961998-07-15015 July 1998 LER 98-010-00:on 980615,TS Required Shutdown Due to Inoperability of TIP Sys Isolation Valve Was Noted.Caused by Improper Installation of TIP Tubing.Reattached Affected Tubing & Inspected Other TIP tubing.W/980715 Ltr ML17284A6731998-07-0101 July 1998 LER 98-009-00:on 980606,nuclear Steam Supply Shutoff Sys Group 3 & 4 Isolations During Testing Was Noted.Caused by Procedural Deficiency.Counseled Individuals Involved in preparation.W/980701 Ltr ML17284A6651998-06-24024 June 1998 LER 98-007-00:on 980530,inadvertent Full Scram & Division 1 ECCS Injection Was Noted.Caused by Failure to Meet Mgt Work Practice Expectation When Encountering Deficient Procedure. Incident Review Board Convened to Review event.W/980624 Ltr ML17284A6641998-06-24024 June 1998 LER 98-008-00:on 980531,inadvertent Full Scram During RPV Leak Testing in Mode 4 Was Noted.Caused by Change in Mgt Techniques.Revised Procedures to Take Into Account Addl Water Head in Pressure Sensing lines.W/980624 Ltr ML17284A6631998-06-19019 June 1998 LER 98-006-00:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of App R Calculations for High Impedance Fault Analysis.Caused Indeterminate. Implemented Procedural Changes Involving Operator Action ML17284A6551998-06-0404 June 1998 LER 98-005-00:on 980506,potential for Failure of RHR Sys Valve to Close on Isolation Signal Was Noted.Caused by Design Deficiency.Caution Tag Was Placed on RHR-V-40 Control Switch to Inform Plant Operators of limitation.W/980604 Ltr ML17284A6421998-06-0101 June 1998 LER 98-004-00:on 980502,determined That Primary Containment Penetration Overcurrent Protection Does Not Meet Reg Guide 1.63 Requirements.Caused by Inadequate Design Changes. Installed Addl Fuse in RHR-MO-9 circuit.W/980601 Ltr ML17292B3281998-04-0909 April 1998 LER 98-002-00:on 980311,reactor Scram & Plant Transient Occurred,Due to Failed Closed Main Steam Isolation Valve. Caused by Loss of Pneumatic Actuating Supply Pressure. Problem Evaluation Request Written for Failure of MS-V-22D ML17292B3291998-04-0909 April 1998 LER 98-003-00:on 980311,WNP-2 Experienced SCRAM Signal as Result of Low Rpv.Caused by Less than post-SCRAM Operational Strategy for Resetting SCRAM Signal in Conditions.Changes in post-SCRAM Operational Strategy implemented.W/980409 Ltr ML17292B2661998-03-0404 March 1998 LER 98-001-00:on 980203,automatic Start of HPCS EDG Was Noted.Caused by Operator Error.Operations Crew Stabilized Plant at Approximately 75% Reactor Power & Investigation of Event Was initiated.W/980304 Ltr ML17292B1111997-11-10010 November 1997 LER 97-011-00:on 971010,HPCS Battery Charger Failed.Caused by Failure of a Phase Firing Control Circuit Board Due to Aging During 7 Yrs of Use.Hpcs Sys Was Immediately Declared inoperable.W/971110 Ltr ML17292B1151997-11-0707 November 1997 LER 97-010-00:on 970906,discovered That TS SR 3.4.5.1 for Identified Portion of RCS Total Leakage Would Not Be Able to Perform within Time Limits of SR 3.0.2.Caused by Inadequate Methods.Method of Meeting SR 3.4.5.1 Established ML17292B0641997-09-24024 September 1997 LER 97-004-01:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Indication of Entry Into Region a of power-to-flow Map.Caused by Inadequate Attention to Detail.Established Event Evaluation teams.W/970924 Ltr ML17292B0241997-08-18018 August 1997 LER 97-009-00:on 970717,discovered Error in Recently Performed Inservice Testing procedure,OSP-TIP/IST-R701. Caused by Procedure Inadequacy.Plant Procedure OSP/TIP/IST-R701 Will Be changed.W/970818 Ltr ML17292B0291997-08-15015 August 1997 LER 97-008-00:on 970716,wire Seal Used to Lock Containment Instrument Air Pressure Control valve,CIA-PCV-2B,found Not Intact.Cause of Misadjustment of CIA-PCV-2B Unknown.Event Will Be Communicated to Plant employees.W/970815 Ltr ML17292B0201997-08-15015 August 1997 LER 97-S01-00:on 970718,failure to Take Compensatory Measure for Inoperative Microwave Security Zone Occurred. Caused by Personnel Error.Training Will Be Conducted W/ Appropriate Members of Security force.W/970815 Ltr ML17292A9481997-07-23023 July 1997 LER 97-007-00:on 970611,voluntary Rept of Automatic Start of DG-1 & DG-2 Was Experienced.Caused by Undervoltage Condition on Electrical Busses SM-7 & SM-8.Circulating Water Pump CW-P-1C Control Switch Placed in pull-to-lock.W/970723 Ltr ML17292A9201997-06-26026 June 1997 LER 97-006-00:on 970527,non-performance of Surveillance Requirement 3.6.1.3.2 for Blind Fanges,Was Noted.Caused Because Misunderstanding of Intent of Specs.Added Five Structural Assemblies for SP.W/970626 Ltr ML17292A8331997-04-28028 April 1997 LER 97-004-00:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Entry Into Region a of power-to-flow Map Following Planned Trip of Single Mfp. Event Evaluation teams,established.W/970428 Ltr ML17292A8311997-04-28028 April 1997 LER 97-005-00:on 970327,valid Reactor Scram Signal Received Due to Low Water Level Condition During Preparations for SRV Testing.Caused by Risks & Consequences of Decisions Not Completely Identified.Restored Water level.W/970428 Ltr ML17292A8251997-04-21021 April 1997 LER 97-003-00:on 970320,notification of Noncompliance W/Ts as TS SRs for Response Time Testing Were Not Being Met for Specified Instrumentation in Rps,Pcis & Eccs.Requested Enforcement Discretion for One Time exemption.W/970421 Ltr ML17292A7431997-03-20020 March 1997 LER 97-002-00:on 970218,determined That Rod Block Monitor (RBM) Calibr Values Were Not Set IAW Tech Specs.Caused by Calibr Procedures Inadequacies.Revised & re-performed RBM Channel Calibr procedures.W/970330 Ltr ML17292A7401997-03-13013 March 1997 LER 97-001-00:on 970211,reactor Water Cleanup Sys Blowdown Flow Isolation Setpoint Was Slightly Above TS Allowable Valve Occurred Due to Calculation Error.Lds Fss LD-FS-15 LD-FS-16 Were Declared inoperable.W/970313 Ltr ML17292A6641997-01-22022 January 1997 LER 96-009-00:on 961220,miscalculation of Instantaneous Overcurrent Relay Settings Resulted in Inoperability of safety-related Equipment.Caused by Utilization of Inappropriate Design.Testing Was completed.W/970122 Ltr ML17292A6461997-01-0606 January 1997 LER 96-008-00:on 961205,failure to Comply with TS Action Requirement for Emergency Core Cooling Sys Actuation Instrumentation Occurred Due to Unidentified Inoperability Condition.Pmr initiated.W/970106 Ltr ML17292A6371996-12-19019 December 1996 LER 96-007-00:on 961122,electrical Breakers Were Not Seismically Qualified in Test/Disconnect Position.Circuit Breaker Mfg Did Not Consider Raced Out Breaker Position During Testing.Relocated Circuit breakers.W/961217 Ltr ML17292A4121996-08-0808 August 1996 LER 96-006-00:on 960709,average Power Range Monitor Rod Block Downscale Surveillance Not Performed Prior to Entry Into Mode 1.Caused by long-standing Misinterpretation of Requirements of Tss.Procedures revised.W/960808 Ltr ML17292A3801996-07-24024 July 1996 LER 96-004-00:on 960624,plant Was Manually Scrammed by Control Room Personnel Due to Reactor Water Level Transient Experienced During Testing of Digital Feedwater Sys.Caused by Programming Error.Sys Was corrected.W/960724 Ltr ML17292A3771996-07-24024 July 1996 LER 96-005-00:on 960624,determined Missed Surveillance Test Re Channel Check of Average Power Range Monitor.Caused by Inadequate Procedures.Revised Surveillance Procedure Re When APRM Checks Must Be performed.W/960724 Ltr ML17292A3641996-07-12012 July 1996 LER 96-003-00:on 960615,required Surveillance Test Not Performed When Required by TS 3.4.1.3.Caused by Inadequate Procedures.Implementing Surveillance Procedure & Reactor Plant Startup Procedures revised.W/960712 Ltr ML17292A3361996-06-20020 June 1996 LER 96-002-00:on 960504,critical Bus SM-8 Lost Power When Supply Breaker 3-8 Tripped.Caused by Personnel Error. Operators Counselled & Procedures revised.W/960620 Ltr ML17292A2861996-05-24024 May 1996 LER 96-001-00:on 960425,inadvertent ESF Actuations Occurred Due to Tripping of Temporary Power Supply to IN-3.Caused by Personnel Error.Operations Restored to IN-3 Loads & Reset ESF actuations.W/960524 Ltr ML17291B0891995-10-19019 October 1995 LER 95-011-00:on 950919,failed to Comply W/Ts SR for RCIC Sys Due to Analysis Deficiency That Resulted in Inadequate Surveillance Test Procedure.Surveillance Procedure Revised to Correct deficiency.W/951019 Ltr ML17291A9021995-07-0707 July 1995 LER 95-010-00:on 950609,HPCS DG Declared Inoperable Due to Discovery That TS Test Method Incomplete.Caused by Inadequate Testing Procedure.Test Procedure for HPCS DG Reviewed & Special Test Procedures written.W/950707 Ltr ML17291A9031995-07-0707 July 1995 LER 95-009-00:on 950607,inadvertent MSIV Closure Occurred During Surveillance Test Due to Poor Communication Between Test Team.Determined That MSIV Closure Not Valid Because Closure Not Triggered by Plant conditions.W/950707 Ltr ML17291A8501995-06-0808 June 1995 LER 95-006-01:on 950405,reactor Scram Occurred During Surveillance Testing Due to Protective Sys Relay Failure. Replaced Failed Relay Before Plant Startup ML17291A8101995-05-12012 May 1995 LER 95-008-00:on 940125,TS Wording Lead to Potential TS Violation.Caused by Lack of Clarity in Ts.Submitted Improved TS for Plant to Provide Addl clarity.W/950512 Ltr ML17291A7841995-05-0505 May 1995 LER 95-007-00:on 950222,emergency Diesel Start Occurred Due to Voltage Transient on BPA Grid.Confirmation Was Received at 17:51 H That Disturbance Had Originated in BPA Grid ML17291A7801995-05-0404 May 1995 LER 95-006-00:on 950405,main Turbine Trip Occurred During Performance of Surveillance Test Due to Protective Sys Relay Failed.Replaced Failed Relay Before Plant startup.W/950504 Ltr ML17291A7851995-05-0303 May 1995 LER 95-005-00:on 950222,inoperable IRM Had Been Relied Upon to Meet TS Requirements During Reactor Startup.Caused by Lack of Neutron Source to Test Instrumentation. Sys Knowledge Gained Will Be incorporated.W/950503 Ltr ML17291A7071995-03-25025 March 1995 LER 95-004-00:on 950226,malfunction in Main Turbine DEH Control Sys Caused All Four High Pressure Turbine Governor Valves to Rapidly Close.Caused by Blown Fuse.Suspected Faulty Circuit Card replaced.W/950325 Ltr ML17291A7011995-03-20020 March 1995 LER 95-002-00:on 950218,automatic Reactor Scram Occurred. Caused by Erroneous Positioning of Control During Performance of Scheduled Periodic Functional Test.Control repositioned.W/950320 Ltr 1999-07-20
[Table view] Category:RO)
MONTHYEARML17292B7421999-07-20020 July 1999 LER 99-001-00:on 990628,ESF Signal Closed All Eight MSIVs While Plant Was Shutdown.Caused by Failure of Relay RPS-RLY-K10D.Subject Relay Was Replaced & Tested on 990630. with 990720 Ltr ML17292B4451998-10-27027 October 1998 LER 98-012-01:on 980715,failure to Comply with Requirements of TS SR 3.8.4.7 Was Noted.Caused by Inadequate Work Practices.Training Session Was Held with Personnel.With 981027 Ltr ML17284A7561998-09-0303 September 1998 LER 98-013-00:on 980805,ESF Actuations Were Noted Due to Deenergization of Vital Electrical Bus SM-8.Caused by Inadequate Direction in Troubleshooting Plan.Will Conduct Training for Engineering Personnel.With 980903 Ltr ML17284A7571998-09-0202 September 1998 LER 98-014-00:on 980807,completion of TS 3.8.1.F Required Shutdown Due to Inoperability of EDG-2 Was Noted.Caused by Degraded Voltage Regulator for DG-2.Replaced Voltage Regulator & Associated Scrs.With 980902 Ltr ML17284A7551998-09-0202 September 1998 LER 98-015-00:on 980808,discovered Reactor Coolant Pressure Boundary Leak During Shutdown Conditions.Caused by Leakage from Socket Weld (Fwb 63) on Elbow Connection.Failed Piping Connection Was Replaced.With 980902 Ltr ML17284A7311998-08-17017 August 1998 LER 98-012-00:on 980716,determined That 24-month SR 3.8.4.7 Had Not Been Fulfilled within Specified Frequency.Caused by Inadequate Work Practices.License Requested & Received Enforcement Discretion Re Battery Svc test.W/980817 Ltr ML17284A7121998-07-23023 July 1998 LER 98-006-01:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of 10CFR50,App R Calculations for High Impedance Faults.Caused by Inadequate Work Practices.Implemented Procedural Changes ML17284A6951998-07-17017 July 1998 LER 98-011-00:on 980617,ECCS Pump Room Flooding Was Noted Due to FP Sys Pipe Break.Caused by Inadequate Design of FP Sys.Detailed Review of FP Sys Design Was Conducted. W/980717 Ltr ML17284A6961998-07-15015 July 1998 LER 98-010-00:on 980615,TS Required Shutdown Due to Inoperability of TIP Sys Isolation Valve Was Noted.Caused by Improper Installation of TIP Tubing.Reattached Affected Tubing & Inspected Other TIP tubing.W/980715 Ltr ML17284A6731998-07-0101 July 1998 LER 98-009-00:on 980606,nuclear Steam Supply Shutoff Sys Group 3 & 4 Isolations During Testing Was Noted.Caused by Procedural Deficiency.Counseled Individuals Involved in preparation.W/980701 Ltr ML17284A6651998-06-24024 June 1998 LER 98-007-00:on 980530,inadvertent Full Scram & Division 1 ECCS Injection Was Noted.Caused by Failure to Meet Mgt Work Practice Expectation When Encountering Deficient Procedure. Incident Review Board Convened to Review event.W/980624 Ltr ML17284A6641998-06-24024 June 1998 LER 98-008-00:on 980531,inadvertent Full Scram During RPV Leak Testing in Mode 4 Was Noted.Caused by Change in Mgt Techniques.Revised Procedures to Take Into Account Addl Water Head in Pressure Sensing lines.W/980624 Ltr ML17284A6631998-06-19019 June 1998 LER 98-006-00:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of App R Calculations for High Impedance Fault Analysis.Caused Indeterminate. Implemented Procedural Changes Involving Operator Action ML17284A6551998-06-0404 June 1998 LER 98-005-00:on 980506,potential for Failure of RHR Sys Valve to Close on Isolation Signal Was Noted.Caused by Design Deficiency.Caution Tag Was Placed on RHR-V-40 Control Switch to Inform Plant Operators of limitation.W/980604 Ltr ML17284A6421998-06-0101 June 1998 LER 98-004-00:on 980502,determined That Primary Containment Penetration Overcurrent Protection Does Not Meet Reg Guide 1.63 Requirements.Caused by Inadequate Design Changes. Installed Addl Fuse in RHR-MO-9 circuit.W/980601 Ltr ML17292B3281998-04-0909 April 1998 LER 98-002-00:on 980311,reactor Scram & Plant Transient Occurred,Due to Failed Closed Main Steam Isolation Valve. Caused by Loss of Pneumatic Actuating Supply Pressure. Problem Evaluation Request Written for Failure of MS-V-22D ML17292B3291998-04-0909 April 1998 LER 98-003-00:on 980311,WNP-2 Experienced SCRAM Signal as Result of Low Rpv.Caused by Less than post-SCRAM Operational Strategy for Resetting SCRAM Signal in Conditions.Changes in post-SCRAM Operational Strategy implemented.W/980409 Ltr ML17292B2661998-03-0404 March 1998 LER 98-001-00:on 980203,automatic Start of HPCS EDG Was Noted.Caused by Operator Error.Operations Crew Stabilized Plant at Approximately 75% Reactor Power & Investigation of Event Was initiated.W/980304 Ltr ML17292B1111997-11-10010 November 1997 LER 97-011-00:on 971010,HPCS Battery Charger Failed.Caused by Failure of a Phase Firing Control Circuit Board Due to Aging During 7 Yrs of Use.Hpcs Sys Was Immediately Declared inoperable.W/971110 Ltr ML17292B1151997-11-0707 November 1997 LER 97-010-00:on 970906,discovered That TS SR 3.4.5.1 for Identified Portion of RCS Total Leakage Would Not Be Able to Perform within Time Limits of SR 3.0.2.Caused by Inadequate Methods.Method of Meeting SR 3.4.5.1 Established ML17292B0641997-09-24024 September 1997 LER 97-004-01:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Indication of Entry Into Region a of power-to-flow Map.Caused by Inadequate Attention to Detail.Established Event Evaluation teams.W/970924 Ltr ML17292B0241997-08-18018 August 1997 LER 97-009-00:on 970717,discovered Error in Recently Performed Inservice Testing procedure,OSP-TIP/IST-R701. Caused by Procedure Inadequacy.Plant Procedure OSP/TIP/IST-R701 Will Be changed.W/970818 Ltr ML17292B0291997-08-15015 August 1997 LER 97-008-00:on 970716,wire Seal Used to Lock Containment Instrument Air Pressure Control valve,CIA-PCV-2B,found Not Intact.Cause of Misadjustment of CIA-PCV-2B Unknown.Event Will Be Communicated to Plant employees.W/970815 Ltr ML17292B0201997-08-15015 August 1997 LER 97-S01-00:on 970718,failure to Take Compensatory Measure for Inoperative Microwave Security Zone Occurred. Caused by Personnel Error.Training Will Be Conducted W/ Appropriate Members of Security force.W/970815 Ltr ML17292A9481997-07-23023 July 1997 LER 97-007-00:on 970611,voluntary Rept of Automatic Start of DG-1 & DG-2 Was Experienced.Caused by Undervoltage Condition on Electrical Busses SM-7 & SM-8.Circulating Water Pump CW-P-1C Control Switch Placed in pull-to-lock.W/970723 Ltr ML17292A9201997-06-26026 June 1997 LER 97-006-00:on 970527,non-performance of Surveillance Requirement 3.6.1.3.2 for Blind Fanges,Was Noted.Caused Because Misunderstanding of Intent of Specs.Added Five Structural Assemblies for SP.W/970626 Ltr ML17292A8331997-04-28028 April 1997 LER 97-004-00:on 970327,plant Operators Manually Scrammed Reactor as Required by TS Due to Entry Into Region a of power-to-flow Map Following Planned Trip of Single Mfp. Event Evaluation teams,established.W/970428 Ltr ML17292A8311997-04-28028 April 1997 LER 97-005-00:on 970327,valid Reactor Scram Signal Received Due to Low Water Level Condition During Preparations for SRV Testing.Caused by Risks & Consequences of Decisions Not Completely Identified.Restored Water level.W/970428 Ltr ML17292A8251997-04-21021 April 1997 LER 97-003-00:on 970320,notification of Noncompliance W/Ts as TS SRs for Response Time Testing Were Not Being Met for Specified Instrumentation in Rps,Pcis & Eccs.Requested Enforcement Discretion for One Time exemption.W/970421 Ltr ML17292A7431997-03-20020 March 1997 LER 97-002-00:on 970218,determined That Rod Block Monitor (RBM) Calibr Values Were Not Set IAW Tech Specs.Caused by Calibr Procedures Inadequacies.Revised & re-performed RBM Channel Calibr procedures.W/970330 Ltr ML17292A7401997-03-13013 March 1997 LER 97-001-00:on 970211,reactor Water Cleanup Sys Blowdown Flow Isolation Setpoint Was Slightly Above TS Allowable Valve Occurred Due to Calculation Error.Lds Fss LD-FS-15 LD-FS-16 Were Declared inoperable.W/970313 Ltr ML17292A6641997-01-22022 January 1997 LER 96-009-00:on 961220,miscalculation of Instantaneous Overcurrent Relay Settings Resulted in Inoperability of safety-related Equipment.Caused by Utilization of Inappropriate Design.Testing Was completed.W/970122 Ltr ML17292A6461997-01-0606 January 1997 LER 96-008-00:on 961205,failure to Comply with TS Action Requirement for Emergency Core Cooling Sys Actuation Instrumentation Occurred Due to Unidentified Inoperability Condition.Pmr initiated.W/970106 Ltr ML17292A6371996-12-19019 December 1996 LER 96-007-00:on 961122,electrical Breakers Were Not Seismically Qualified in Test/Disconnect Position.Circuit Breaker Mfg Did Not Consider Raced Out Breaker Position During Testing.Relocated Circuit breakers.W/961217 Ltr ML17292A4121996-08-0808 August 1996 LER 96-006-00:on 960709,average Power Range Monitor Rod Block Downscale Surveillance Not Performed Prior to Entry Into Mode 1.Caused by long-standing Misinterpretation of Requirements of Tss.Procedures revised.W/960808 Ltr ML17292A3801996-07-24024 July 1996 LER 96-004-00:on 960624,plant Was Manually Scrammed by Control Room Personnel Due to Reactor Water Level Transient Experienced During Testing of Digital Feedwater Sys.Caused by Programming Error.Sys Was corrected.W/960724 Ltr ML17292A3771996-07-24024 July 1996 LER 96-005-00:on 960624,determined Missed Surveillance Test Re Channel Check of Average Power Range Monitor.Caused by Inadequate Procedures.Revised Surveillance Procedure Re When APRM Checks Must Be performed.W/960724 Ltr ML17292A3641996-07-12012 July 1996 LER 96-003-00:on 960615,required Surveillance Test Not Performed When Required by TS 3.4.1.3.Caused by Inadequate Procedures.Implementing Surveillance Procedure & Reactor Plant Startup Procedures revised.W/960712 Ltr ML17292A3361996-06-20020 June 1996 LER 96-002-00:on 960504,critical Bus SM-8 Lost Power When Supply Breaker 3-8 Tripped.Caused by Personnel Error. Operators Counselled & Procedures revised.W/960620 Ltr ML17292A2861996-05-24024 May 1996 LER 96-001-00:on 960425,inadvertent ESF Actuations Occurred Due to Tripping of Temporary Power Supply to IN-3.Caused by Personnel Error.Operations Restored to IN-3 Loads & Reset ESF actuations.W/960524 Ltr ML17291B0891995-10-19019 October 1995 LER 95-011-00:on 950919,failed to Comply W/Ts SR for RCIC Sys Due to Analysis Deficiency That Resulted in Inadequate Surveillance Test Procedure.Surveillance Procedure Revised to Correct deficiency.W/951019 Ltr ML17291A9021995-07-0707 July 1995 LER 95-010-00:on 950609,HPCS DG Declared Inoperable Due to Discovery That TS Test Method Incomplete.Caused by Inadequate Testing Procedure.Test Procedure for HPCS DG Reviewed & Special Test Procedures written.W/950707 Ltr ML17291A9031995-07-0707 July 1995 LER 95-009-00:on 950607,inadvertent MSIV Closure Occurred During Surveillance Test Due to Poor Communication Between Test Team.Determined That MSIV Closure Not Valid Because Closure Not Triggered by Plant conditions.W/950707 Ltr ML17291A8501995-06-0808 June 1995 LER 95-006-01:on 950405,reactor Scram Occurred During Surveillance Testing Due to Protective Sys Relay Failure. Replaced Failed Relay Before Plant Startup ML17291A8101995-05-12012 May 1995 LER 95-008-00:on 940125,TS Wording Lead to Potential TS Violation.Caused by Lack of Clarity in Ts.Submitted Improved TS for Plant to Provide Addl clarity.W/950512 Ltr ML17291A7841995-05-0505 May 1995 LER 95-007-00:on 950222,emergency Diesel Start Occurred Due to Voltage Transient on BPA Grid.Confirmation Was Received at 17:51 H That Disturbance Had Originated in BPA Grid ML17291A7801995-05-0404 May 1995 LER 95-006-00:on 950405,main Turbine Trip Occurred During Performance of Surveillance Test Due to Protective Sys Relay Failed.Replaced Failed Relay Before Plant startup.W/950504 Ltr ML17291A7851995-05-0303 May 1995 LER 95-005-00:on 950222,inoperable IRM Had Been Relied Upon to Meet TS Requirements During Reactor Startup.Caused by Lack of Neutron Source to Test Instrumentation. Sys Knowledge Gained Will Be incorporated.W/950503 Ltr ML17291A7071995-03-25025 March 1995 LER 95-004-00:on 950226,malfunction in Main Turbine DEH Control Sys Caused All Four High Pressure Turbine Governor Valves to Rapidly Close.Caused by Blown Fuse.Suspected Faulty Circuit Card replaced.W/950325 Ltr ML17291A7011995-03-20020 March 1995 LER 95-002-00:on 950218,automatic Reactor Scram Occurred. Caused by Erroneous Positioning of Control During Performance of Scheduled Periodic Functional Test.Control repositioned.W/950320 Ltr 1999-07-20
[Table view] Category:TEXT-SAFETY REPORT
MONTHYEARML17284A9001999-10-31031 October 1999 Rev 0 to COLR 99-15, WNP-2 Cycle 15,COLR GO2-99-177, LER 99-S01-00:on 990903,failure to Take Compensatory Measure within Required Time Upon Failure of Isolation Zone Microwave Unit,Was Noted.Caused by Personnel Error.Provided Refresher Training on Compensatory Measures.With1999-10-0101 October 1999 LER 99-S01-00:on 990903,failure to Take Compensatory Measure within Required Time Upon Failure of Isolation Zone Microwave Unit,Was Noted.Caused by Personnel Error.Provided Refresher Training on Compensatory Measures.With ML17284A8941999-09-30030 September 1999 Monthly Operating Rept for Sept 1999 for WNP-2.With 991012 Ltr ML17284A8801999-08-31031 August 1999 Monthly Operating Rept for Aug 1999 for WNP-2.With 990910 Ltr ML17284A8691999-07-31031 July 1999 Monthly Operating Rept for July 1999 for WNP-2.With 990813 Ltr ML17292B7421999-07-20020 July 1999 LER 99-001-00:on 990628,ESF Signal Closed All Eight MSIVs While Plant Was Shutdown.Caused by Failure of Relay RPS-RLY-K10D.Subject Relay Was Replaced & Tested on 990630. with 990720 Ltr ML17292B7271999-06-30030 June 1999 Monthly Operating Rept for June 1999 for WNP-2.With 990707 Ltr ML17292B6961999-05-31031 May 1999 Monthly Operating Repts for May 1999 for WNP-2.With 990608 Ltr ML17292B6641999-04-30030 April 1999 Monthly Operating Rept for Apr 1999 for WNP-2.With 990507 Ltr ML17292B6391999-03-31031 March 1999 Monthly Operating Rept for Mar 1999 for WNP-2.With 990413 Ltr ML17292B5871999-02-28028 February 1999 Monthly Operating Rept for Feb 1999 for WNP-2.With 990311 Ltr ML17292B5571999-01-31031 January 1999 Monthly Operating Rept for Jan 1999 for WNP-2.With 990210 Ltr ML17292B5621999-01-31031 January 1999 Rev 1 to COLR 98-14, WNP-2 Cycle 14 Colr. ML17292B5341999-01-15015 January 1999 Part 21 Rept Re Incorrect Modeling of BWR Lower Plenum Vol in Bison.Defect Applies Only to Reload Fuel Assemblies Currently in Operation at WNP-2.BISON Code Model for WNP-2 Has Been Revised to Correct Error ML17292B5331999-01-15015 January 1999 Part 21 Rept Re XL-S96 CPR Correlation for SVEA-96 Fuel. Defect Applies Only to WNP-2,during Cycles 12,13 & 14 Operation.Evaluations of Defect Performed by ABB-CE ML17292B4791998-12-31031 December 1998 Washington Public Power Supply Sys 1998 Annual Rept. with 981215 Ltr ML17292B5351998-12-31031 December 1998 Monthly Operating Rept for Dec 1998 for WNP-2.With 990112 Ltr ML17292B5741998-12-31031 December 1998 WNP-2 1998 Annual Operating Rept. with 990225 Ltr ML17284A8231998-11-30030 November 1998 Monthly Operating Rept for Nov 1998 for WNP-2.With 981207 Ltr ML17284A8081998-10-31031 October 1998 Monthly Operating Rept for Oct 1998 for WNP-2.With 981110 Ltr ML17292B4451998-10-27027 October 1998 LER 98-012-01:on 980715,failure to Comply with Requirements of TS SR 3.8.4.7 Was Noted.Caused by Inadequate Work Practices.Training Session Was Held with Personnel.With 981027 Ltr ML17284A7831998-09-30030 September 1998 Monthly Operating Rept for Sept 1998 for WNP-2.With 981007 Ltr ML17284A7491998-09-10010 September 1998 WNP-2 Inservice Insp Summary Rept for Refueling Outage RF13 Spring,1998. ML17284A7561998-09-0303 September 1998 LER 98-013-00:on 980805,ESF Actuations Were Noted Due to Deenergization of Vital Electrical Bus SM-8.Caused by Inadequate Direction in Troubleshooting Plan.Will Conduct Training for Engineering Personnel.With 980903 Ltr ML17284A7571998-09-0202 September 1998 LER 98-014-00:on 980807,completion of TS 3.8.1.F Required Shutdown Due to Inoperability of EDG-2 Was Noted.Caused by Degraded Voltage Regulator for DG-2.Replaced Voltage Regulator & Associated Scrs.With 980902 Ltr ML17284A7551998-09-0202 September 1998 LER 98-015-00:on 980808,discovered Reactor Coolant Pressure Boundary Leak During Shutdown Conditions.Caused by Leakage from Socket Weld (Fwb 63) on Elbow Connection.Failed Piping Connection Was Replaced.With 980902 Ltr ML17284A7681998-08-31031 August 1998 Monthly Operating Rept for Aug 1998 for WNP-2.With 980915 Ltr ML17284A7311998-08-17017 August 1998 LER 98-012-00:on 980716,determined That 24-month SR 3.8.4.7 Had Not Been Fulfilled within Specified Frequency.Caused by Inadequate Work Practices.License Requested & Received Enforcement Discretion Re Battery Svc test.W/980817 Ltr ML17284A7261998-07-31031 July 1998 Monthly Operating Rept for July 1998 for WNP-2.W/980810 Ltr ML17284A7121998-07-23023 July 1998 LER 98-006-01:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of 10CFR50,App R Calculations for High Impedance Faults.Caused by Inadequate Work Practices.Implemented Procedural Changes ML17284A6951998-07-17017 July 1998 LER 98-011-00:on 980617,ECCS Pump Room Flooding Was Noted Due to FP Sys Pipe Break.Caused by Inadequate Design of FP Sys.Detailed Review of FP Sys Design Was Conducted. W/980717 Ltr ML17284A6961998-07-15015 July 1998 LER 98-010-00:on 980615,TS Required Shutdown Due to Inoperability of TIP Sys Isolation Valve Was Noted.Caused by Improper Installation of TIP Tubing.Reattached Affected Tubing & Inspected Other TIP tubing.W/980715 Ltr ML17284A6731998-07-0101 July 1998 LER 98-009-00:on 980606,nuclear Steam Supply Shutoff Sys Group 3 & 4 Isolations During Testing Was Noted.Caused by Procedural Deficiency.Counseled Individuals Involved in preparation.W/980701 Ltr ML17284A6751998-06-30030 June 1998 Ro:On 980617,flooding of RB Northeast Stairwell with Consequential Flooding of Two ECCS Pump Rooms.Caused by Inadequate Fire Protection Sys Design.Pumped Out Water from Affected Areas to Point Below Berm Areas of Pump Rooms ML17284A6641998-06-24024 June 1998 LER 98-008-00:on 980531,inadvertent Full Scram During RPV Leak Testing in Mode 4 Was Noted.Caused by Change in Mgt Techniques.Revised Procedures to Take Into Account Addl Water Head in Pressure Sensing lines.W/980624 Ltr ML17284A6651998-06-24024 June 1998 LER 98-007-00:on 980530,inadvertent Full Scram & Division 1 ECCS Injection Was Noted.Caused by Failure to Meet Mgt Work Practice Expectation When Encountering Deficient Procedure. Incident Review Board Convened to Review event.W/980624 Ltr ML17284A6631998-06-19019 June 1998 LER 98-006-00:on 980520,discovered Discrepancies in Low Voltage Bus Calculations During Review of App R Calculations for High Impedance Fault Analysis.Caused Indeterminate. Implemented Procedural Changes Involving Operator Action ML17284A6551998-06-0404 June 1998 LER 98-005-00:on 980506,potential for Failure of RHR Sys Valve to Close on Isolation Signal Was Noted.Caused by Design Deficiency.Caution Tag Was Placed on RHR-V-40 Control Switch to Inform Plant Operators of limitation.W/980604 Ltr ML17284A6421998-06-0101 June 1998 LER 98-004-00:on 980502,determined That Primary Containment Penetration Overcurrent Protection Does Not Meet Reg Guide 1.63 Requirements.Caused by Inadequate Design Changes. Installed Addl Fuse in RHR-MO-9 circuit.W/980601 Ltr ML17284A6491998-05-31031 May 1998 Rev 0 to COLR 98-14, WNP-2,Cycle 14 Colr. ML17292B4031998-05-31031 May 1998 Monthly Operating Rept for May 1998 for WNP-2.W/980608 Ltr ML17292B3921998-04-30030 April 1998 Monthly Operating Rept for Apr 1998 for WNP-2.W/980513 Ltr ML17292B3291998-04-0909 April 1998 LER 98-003-00:on 980311,WNP-2 Experienced SCRAM Signal as Result of Low Rpv.Caused by Less than post-SCRAM Operational Strategy for Resetting SCRAM Signal in Conditions.Changes in post-SCRAM Operational Strategy implemented.W/980409 Ltr ML17292B3281998-04-0909 April 1998 LER 98-002-00:on 980311,reactor Scram & Plant Transient Occurred,Due to Failed Closed Main Steam Isolation Valve. Caused by Loss of Pneumatic Actuating Supply Pressure. Problem Evaluation Request Written for Failure of MS-V-22D ML17292B3371998-03-31031 March 1998 Monthly Operating Rept for Mar 1998 for WNP-2.W/980409 Ltr ML17292B2641998-03-0404 March 1998 Performance Self Assessment,WNP-2. ML17292B2661998-03-0404 March 1998 LER 98-001-00:on 980203,automatic Start of HPCS EDG Was Noted.Caused by Operator Error.Operations Crew Stabilized Plant at Approximately 75% Reactor Power & Investigation of Event Was initiated.W/980304 Ltr ML17292B2911998-02-28028 February 1998 Monthly Operating Rept for Feb 1998 for WNP-2.W/980313 Ltr ML17284A7971998-02-17017 February 1998 Rev 28 to Operational QA Program Description, WPPSS-QA-004.With Proposed Rev 29 ML17292B3591998-02-12012 February 1998 WNP-2 Cycle 14 Reload Design Rept. 1999-09-30
[Table view] |
Text
ACCELERATED D STRIBUTION DEMONS TION SYSTEM 1 4 REGULATORY INFORMATION DISTRIBUTION SYSTEM (RIDS)
ACCESSION NBR: 9006270256 DOC. DATE: 90/06/19 NOTARIZED: NO DOCKET FACIL:50-397 WPPSS Nuclear Project, Unit 2, Washington Public Powe 05000397 AUTH. NAME AUTHOR AFFILIATION ARBUCKLE,J.D. Washington Public Power Supply System POWERS,C.M. Washington Public Power Supply System RECIP.NAME . RECIPIENT AFFILIATION
SUBJECT:
LER 89-040-01':on 890919,standby gas treatment sys capability not within license basis consideration.
W/9 ltr.
DISTRIBUTION CODE: IE22T COPIES RECEIVED:LTR ENCL SIZE:
TITLE: 50.73/50.9 Licensee Event Report (LER), Incident Rpt, etc.
NOTES'ECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD5 LA 1 PD5 PD 1 1 SAMWORTH,R 1 1 INTERNAL: ACNW 2 2 ACRS 2 2 AEOD/DOA 1 1 AEOD/DS P/TPAB 1 1 AEOD/ROAB/ DS P 2 2 DEDRO 1 1 NRR/DET/ECMB 9H 1 1 NRR/DET/EMEB9H3 1 1 NRR/DLPQ/LHFB11 1 1 NRR/DLPQ/LPEB10 1 1 NRR/DOEA/OEAB11 1 1 NRR/DREP/PRPB11 2 2 NRR/DST/SELB 8D 1 1 NRR/DST/SICB 7E 1 1 NRR~Sg/:S PEED':~ 1 1 NRR/DST/SRXB 8E 1 1 1 1 RES/DSIR/EIB 1 1 RGN5 FILE 01 1 1 EXTERNAL EGGG STUART i V A 4 4 L ST LOBBY WARD 1 1 LPDR 1 1 NRC PDR 1 -
1 NSIC MAYS,G 1 1 NSIC MURPHY,G.A 1 1 NUDOCS FULL TXT 1 1 rv~
t oust'o 2<~9 NOTE TO ALL "RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE! CONTACT THE DOCUMENT CONTROL DESK, ROOM Pl-37 (EXT. 20079) TO ELIMINATEYOUR NAME FROM DISTRIBUTION LISTS FOR DOCUMENTS YOU DON'T NEED!
FULL TEXT CONVERSION REQUIRED TOTAL NUMBER OF COPIES REQUIRED: LTTR 36 ENCL 36
WASHINGTON PUBLIC POWER SUPPLY SYSTEM P.O. Box 96B ~ 3000 George Washington Way ~ Richland, Washington 99352 Docket No. 50-397 June 19, 1990 Document Control Desk U.S. Nuclear Regulatory Commission Washington, D.C. 20555
Subject:
NUCLEAR PLANT NO. 2 LICENSEE EVENT REPORT NO. 89-040-01
Dear Sir:
Transmitted herewith is Licensee Event Report No. 89-040-01 for the WNP-2 Plant. This report is submitted in response to the report requirements of 10CFR50.73 and discusses the items of reportability, corrective action taken, and action taken to preclude recurrence.
'ery,t.ruly yours, gttt/.,:.,
C. H. Powers (H/D 927H)
WNP-2 Plant Hanager CHP:lr
Enclosure:
Licensee Event Report No. 89-040-01 cc: Hr. John B. Hartin, NRC Region V Hr. C. J. Bosted, NRC Site (H/D 901A)
INPO Records Center Atlanta, GA Hs. Dottie Sherman, ANI Hr. D. L. Williams, BPA (H/D 399)
NRC FORM 366 , U.S. NUCLEAR REGULATORY COMMISSION (64)9) APPROVED OMB NO. 3(504)104 EXPIRES: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REOUEST: 50.0 HRS. FORWARD LICENSEE EVENT REPORT (LER) COMMENTS REGARDING BURDEN ESTIMATE To THE RECORDS AND REPORTS MANAGEMENT BRANCH IP4I30), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (31500104), OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) PA E 3 Washin ton Nuclear Plant - Unit 2
'"" '" Standby Gas Treatment ystem 0 s 0 o 03 97 ior0 8 apa i i y o i in i cense asi s onsi era i on for Secondary Containment Performance Under Certain Conditions Due to Design EVENT DATE (6) LER NUMBER (6) REPORT DATE I7) OTHER FACILITIES INVOLVED (SI MONTH DAY YEAR i%+ SEOUENZrAL REYrSK FACILITYNAMES DOCKET NUMBER(SI YEAR ?K~4 NUMSER gg NUMSER MoNTH OAY YEAR 0 5 0 0 0 0 919 8 9 8 9 040 01 06 19 9 0 0 5 0 0 0 OPERATING THIS REPORT IS SUBMITTED PURSUANT To THE RLOUIREMENTS OF 10 CFR (): /Check one or morr ot the /or/or>>inc/ (ill MOOE (9) 20.402(5) 20A05(cl 60.73( ~ l(2)liv) 73.71(tr)
POWE R 20A05 ( ~ IllI I I) 60.35(cl(1) 50.73( ~ )l2)(v) 73.71(cl LEYEL 1 0 0 20.405(e)(1) (ill 50.35(c I (2 I 50.73( ~ ) (2) I vii) oTHER /specify In Aorrrecr oerovv mr/ In Test, NRC Form 20.405( ~ ) (1) I(ill 60.73( ~ I (2) IB 50,73( ~ ) (2) ( viiil (AI SSSA/
20A05(e ) (I ) (iv) 50.73( ~ l(2) liil 50.73(e)(2)(vlii)IB) 20A05(el(1 Hvl 50.73(el(2) liiil 60.73( ~ )I2)ls)
LICENSEE CON1'AC'T FOR THIS LER (12)
NAME TELEPHONE NUMBER AREA CODE J . D. Arbuckle Com liance En ineer 50 937 7- 211 5 COMPLETE ONE LINE FOR EACH COMPONENT FAILURE DESCRIBED IN THIS REPOR'7 (13)
CAUSE SYSTEM COMPONENT MANUFAC REPORTABLE MANUFAC EPORTABLE gS Sr CAUSE SYSTEM COMPONENT TURER TO NPRDS
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On September 19, 1989 it was determined by Engineering analysis that under certain meteorological conditions (moderate wind and low temperature), coincident with a DBA LOCA and assumed failure of one train of the Standby Gas Treatment (SGT) system, a situation would be created that is not within the licensing basis consideration for Secondary Containment performance. The Engineering analysis was performed as a further corrective action for LER 88-023.
The QNP-2 FSAR states that the Secohdary Containment will be maintained at=minimum differential pressure of -0.25H W.G. following a postulated LOCA, and that this differential will be established within two minutes following the accident. Recent analysis, based upon Standby Gas Treatment, Secondary Containment, Standby Service Water and weather modeling, shows that during post-LOCA, or adverse weather, differential pressure of the'Secondary Containment may not always meet the FSAR commitments. Certain combinations of post-LOCA single active failures and winter conditions adversely affect Secondary Containment and, as a result, increase Secondary Containment leakage.
NRC Form 366 (64)9)
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (669) APPROVED OMB NO. 31500)04 EXPIRES: 4/30/92 4ATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EV REPORT (LER) INFORMATION COLLECTION REQUEST: 60A) HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (P.530), U.S. NUCLEAR REGULATORY COMMISSION. WASHINGTON. OC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (31504104). OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON,DC20503.
FACILITY NAME (1) DOCKET NUMBER (2) PAGE (3)
LER NUMBER (6)
YEAR ~g: SEOUENTIAL REVISION NUMBER NUMBER Mashin ton Nuclear Plant TEXT /I/ moro 4/>>ce /4 rer/oired, ore eddie'ooe///RC %%dnrr
- Unit 366A'4/ () 7) 2 o s << o 9 7 9 0 0 4 0 010 2 oFO 8 On. January 8, 1990, as a result of in-depth reviews of calculations pertinent to secondary containment accident performance, a problem with the meteorology data presented in FSAR Amendment 36 was discovered. It was determined that the values for the source term dispersion pattern relative concentration factor, X/g, were specified incorrectly in FSAR Amendment 36.
As an immediate corrective action, a Justification for Continued Operation (JCO) was performed and concluded that operation of the Plant can continue while final resolution of this issue is achieved. In addition, this. situation was reviewed relative to the requirements of 10CFR50.59 and it was determined that it represents an unreviewed safety question. Accordingly, the NRC was formally notified of this determination.
As a further corrective action, a test was run to confirm the leakage value used for the JCO. In addition, Design Basis changes will be evaluated to provide an SGT system that allows for adequate filtering of Secondary Containment for applicable meteorological conditions, and system draw down time, so as to meet 10CFR100 and GDC 1 9 limits, while taking credit for suppression pool scrubbing as allowed by Standard Review Plan 6.5.5.
This event did not affect the health and safety of either the public or Plant personnel.
Plant Conditions Power Level - lOOX Plant Mode- - 1 (Power Operation)
Event Descri tion On September 19, 1989, it was determined by Engineering analysis that under certain meteorological conditions (moderate wind and low temperature), coincident with a DBA LOCA and assumed failure of one train of the Standby Gas Treatment (SGT) System, a situation would be created that is not within the licensing basis consideration for Secondary Containment performance. The Engineering analysis was performed as a further corrective action for LER 88-023, HTechnical Specifiation Violation of Secondary Containment to Outside Differential Pressure Caused by Design due to Programmatic Errors."
NRC Form 366A (64)9)
NAC FORM 366A U.S. NUCLEAR AEGULATOAYCOMMISSION (6$ 9I APPROVED 0MB NO. 31500106 E XP I R ES: 4(30(92 MATEO BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVE REPORT (LER) E INFORMATION COLLECTION REOUESTI 50AI HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (P430L U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON. OC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (31500(041. OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1( DOCKET NUMBER (2( LEA NUMBER (6( PAGE (3I YEAR ~(@ SEOUENTIAL NUM SEA REVISION NUMBER Washin ton Nuclear Plant TEXT Irfmoro spooo is ror(rrirrrd
- Unit 0>> oddirlonsl NRC Form 366ABI (17(
2 o s << o 3 9 7 9 0 0 4 0010 3 oF 0= 8 The MNP-2 FSAR states that. the Secondary Containment will be maintained at minimum differential pressure of -0.25H W.G. following a postulated LOCA, and that this differential will be established within two minutes following the accident. Recent analysis, based upon Standby Gas Treatment, Secondary Containment, Standby Service Water (SSW), and weather modeling, shows that during post-LOCA, or adverse weather, differential pressure of the Secondary Containment may not always meet the FSAR com-mitments. Certain combinations of post-LOCA single active failures and winter conditions adversely affect Secondary Containment and, as a result, increase Secondary Containment leakage.
The analysis uses the lowest monthly average temperature for January of 12/F in combination with the highest average monthly wind for January of 1 0.3 mph. On the average, temperature is below 12/F approximately 1.6% of the calendar year, and below 0/F approximately 0.1% of the calendar year. Wind conditions above 10.3 mph will probably provide sufficient dispersion to preclude the need far maintaining the
-0.25H differential and; therefore, negates designing the SGT for worst case wind conditions.
Mind increases the demand on the SGT to hold the leeward side and roof of the Reactor Building sufficiently negative while simultaneously increasing the differential pressure and, thus, the inleakage on the windward side of the building. Differen- tial temperature between the inside and outside of the building creates a differential pressure gradient from the bottom to the top of the Secondary Containment due to the density difference of the air inside and outside the building during cold outside conditions. As a result, the lower portion of the building must be held at a high differential pressure (up to -0.75H) to assure that a -0.25R differential exists at the building roofline. This overall greater differential pressure proportionally increases building inleakage. The effects of wind and winter temperatures result =in the inability to hold the upper portion of the Secondary Containment at a -0.25H differential in cold and mildly windy weather, and lengthens the time required to reach -0.25H differential in warmer and less wing weather.
Analysis shows that the time required to reach the steady state condition is a function of the assumed meteorological conditions at the time of a postulated LOCA, type of single active failure coincident with the LOCA, and the Standby Service Water (SSW) temperature. The transient analysis clearly indicates that the limiting single active failure is the assumed loss of one SGT train. Based upon single train design basis SGT flow and maximum Technical Specification allowable Secondary Con-tainment leakage, the uppermost inside surface areas of the Reactor Building cannot be maintained at a -0.25 '.G. with respect to atmospheric pressure during low temperature and high wind conditions. High SSW water temperature acts to extend the time required to reach a steady state condition, but does not effect the final steady state differential pressure.
NRC Form 366A (6J(9(
NRC FORM 366A U.S, NUCLEAR REGULATORY COMMISSION (64)9) APPROVED OMB NO. 31500104 EXP IR ES: 4i30i92 rMATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EV REPORT (LER) E INFORMATION COLI.ECTION REOVEST: 60A) HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION ANO REPORTS MANAGEMENT BRANCH IP.530), U.S. NUCLEAR REGULATORY COMMISSION. WASHINGTON, OC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (31500104), OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (11 DOCKET NUMBER (21 LER NUMBER (6) PAGE (3)
YEAR @8 SEOVSNTIAL NUMBER REVISION NVM ER Washin ton Nuclear Plant - Unit 2 97 90 0 4 0 OF TEXT (Ji moro spssoir rsr)oirod, oss sddidonsl HRC Form 366A'sl (17)
With two fans redundantly powered in each train, the SGT is not susceptible to many of the single active failures that have a higher probability of occurrence relative to other events, e.g., failure of an emergency diesel generator to start. If one train does fail to start automatically, remote manual initiation and process monitoring can occur through the control room. A design review of the system to determine the susceptibility of an SGT train to single failure has not been performed. Until that occurs, the likelihood of failure, or what would be necessary to remedy failure susceptibilities, is not known. (Local control is not possible due to the post-LOCA radiation fields that are postulated to be present in the vicinity of the SGT trains.) From a failure analysis perspective, the SGT train design at WNP-2 does have features that provide more reliable operation than are dictated by the minimum design requirements that allow for satisfying single failure criterion by the existence of a redundant train.
Testing conducted during the past calendar year of SGT flow/differential pressure capability, and testing of Secondary Containment integrity show that the SGT is capable of performance beyond design basis requirements, and that the Secondary Containment is significantly more leak-tight than required by Technical Specifications. Actions have been taken over the past twelve months to further tighten the Secondary Containment boundary against leakage, e.g., Reactor Building Exhaust and Outside Air (REA and ROA) isolation valve seals have been replaced and the railroad bay door seals have been adjusted. Reanalysis using documented actual performance values for SGT flow capability and Secondary Containment leakage shows that post-LOCA pressure stabilizes at -0.32R with an outside temperature of 12/F with a coincident 10.3 mph wind, which is well below the required -0.25". However, the -0.25" level is not reached for approximately 3.5 minutes after the accident.
Additional margin to the design basis requirements is also available from the actual leakage performance of the Primary Containment. Table 1 outlines the results of analysis based upon licensing basis SGT and Secondary Containment performance fol-lowed by reanalysis results based on realistic SGT and Secondary Containment performance.
Table 1 also demonstrates that the plant can be maintained at the required negative pressures (albeit the time is greater than two minutes) with the current leak-tightness of the Secondary Containment and SGT capability at very low winter temperatures, i .e., -8/F with a 1 0 mph wind, and -23/F without wind. This i s obtained provided that the leak-tightness of Secondary Containment and/or the flow capability of SGT do not degrade by more than 5%, a differential of -0.25R can be maintained at 12/F with a 10 mph wind. Requirements for residence time in the SGT charcoal filters is met with at the 5600 cfm flowrate for design basis active and passive failure scenarios.
Provided that the SGT set point pressure is sufficiently negative, the existing SGT pressure control loop instrumentation will assure that the SGT trains operate at 5600 cfm flow as required during all meteorological conditions. Exisitng loop instrumentation controls Secondary Containment pressure during windy conditions up to existing REA or SGT capacity.
NRC Form 366A (64)9)
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (64)9) APPROVED OMB NO. 31504)104 EXPIRES: 4/30/92 LICENSEE EV ,4ATED BURDEN PER RESPONSE TO COMPLY WTH THIS REPORT (LER) INFOAMATION COLLECTION REQUESTI 60A) HAS. FORWARD COMMENTS REGARDING BUADEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (P4301, U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (31604)104). OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
YEAR < SEOVSNTIAL gag( REVISION
~~<? NVMSSR ~ OS NUM 8 SR Plant - U i 0 5 0 0 0 OF TEXT ///more 4/>>Oe /4 reqrrr'red, Iree edd/rr'or>>l NRC Form 366AB/ (17)
Table 1 Parametric Evaluation of Secondary Containment/SGT Performance Sec. Roof Line Time To Outside Wind SGT Cont. Stdy State Reach Evaluation Description Temp Speed Flow Leakage Pressure -0.25"
('F) (mph) (cfm) (cfm) (AH20) (minutes)
Design Basis 'Performance of SGT and Secondary Containment 12 10. 3 4460 2240 -0. 02 Never Realistic Secondary Containment 12 1 0.3 4460 1475 -0.156 Never Leakage, Design Basis SGT Flow Design Basis Sec. Cont. Leakage, Realistic SGT Capability 12 1 0. 3 5600 2240 -0. 12 Never Realistic Sec. Containment and Realistic SGT Capability 12 10;3 5600 1475 -0.323 3.5 Reanalysis For Coldest Temperature Capability Realistic Sec. Containment and Realistic SGT Capability -23 5600 1475 -0.25 10 Realistic Sec. Containment and Realistic SGT Capability 10.3 5600 1475 -0.25 10 Reanalysis With 5X Margin Realistic Sec. Containment and Real istic SGT Capabil i ty 12 10. 3 5320 1475 -0. 282 Realistic Sec. Containment and Realistic SGT Capability 12 10.3 5600 1549, -0.295 3.6 On January 8, 1990, as a result of in-depth reviews of previous calculations pertinent to secondary containment accident performance, a problem with the meteorology data presented in FSAR Amendment 36 was discovered. It was determined that the values for the source term dispersion pattern relative concentration factor, X/g, were specified .incorrectly in FSAR Amendment 36. The error occurred as a result of incorrect input data used when the atmospheric dispersion calculation model was changed to comply with NRC Regulatory Guide 1.145.
NRC Form 366A (689)
NRC FORM 366A U.S. NUCLEAR AEGULATORY COMMISSION (6$ 9) APPROVED OMB NO. 31600104 E XP I R ES: 4/30/92 4ATED BURDEN PEA RESPONSE TO COMPLY WTH THIS LICENSEE EVE REPORT (LER) ES INFORMATION COLLECTION REQUEST: 500 HRS. FOAWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND AEPOATS MANAGEMENT BRANCH (P.530), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO 1ME PAPERWORK REDUCTION PROJECT 131500104), OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) PAGE (3)
LEA NUMBER (6)
Pip> SEOUENTIAL:~dC REVISION NUMBER NUMBER Washington Nuclear Plant TEXT /// mare epeoe /4>>r/u/red, u>> addio)roe/NRC %%dnn
- Unit 3//MS / ()7) 2 o 5 << o 3 9 7 9 0 0 4 0 0 1 OF A review, of the previosly completed JCO was conducted which resulted in the conclusion that, even with the correct X/g values inserted, both offsite and onsite post accident doses remain below 10CFR100 limits.'lthough this discovery does not present any new instance of reportability, this information is being provided on a voluntary basis as an update on the WNP2 Secondary Containment Performance problem originally reported in this LER. This information was also made available during a recent presentation made by Sypply System Generation Engineering to the Nuclear Regulatory Commission NRR Branch on January 16, 1990.
Immediate Corrective Action A Justification for Continued Operation (JCO) was performed for WNP-2. The conclusion of the JCO is that operation of the Plant can continue while final resolution of this issue is achieved.
On January 10, 1990, the previously prepared JCO was revised to include the effects of the corrected X/I) values. The conclusion of this revised JCO remains that the the operation of the Plant can continue while final resolution -is achieved.
I Further Eva1uati on and Correc ti ve Acti on A. Further Evaluation
- 1. This event is reportable under 10CFR50. 73(a)(2)(ii)(B) as a condition outside of the Plant design basis.
- 2. The cause of this event is design related in that inadequate design criteria were used by the Architect/Engineer (Burns and Roe, Inc. ) to determine SGT draw down time.
- 3. Current NRC requirements for radiological analysis do not allow SGT credit until a full -0.25H differential pressure is established at all Secondary Containment boundary surfaces. A review of existing radiological anlayses indicates that both the post-LOCA offsite and control room doses will increase as a result of delayed reestablishment (beyond two minutes) of the -0.25H differential. However, reanalysis using current rules (Standard Review Plan 6. 5. 5) that allow credit for iodine scrubbing within the suppression pool are expected to result in offsite doses equivalent to those outlined by the FSAR assuming a ten minute "no SGT credit" period to reestablish the full -0.25". The current condition of the SGT and Secondary Containment do not meet the FSAR description under all reasonable environmental conditions; however, the resultant doses are within the 10CFR100 and GDC 19 requirements.
NRC Form 366A (64)9)
NRC FORM 366A U.S. NUCLEAR REGULATORY COMMISSION (6 J)9) APPROVED OMB NO. 31500104 EXPIRES: e/30/92 ES ATED BURDEN PER RESPONSE TO COMPLY WTH THIS LICENSEE EVE REPORT (LER) INFORMATION COLLECTION REOUEST: 503) HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS TEXT CONTINUATION AND REPORTS MANAGEMENT BRANCH (P.530), U.S. NUCLEAR REGULATORY COMMISSION, WASHINGTON, DC 20555, AND TO THE PAPERWORK REDUCTION PROJECT (31504104). OFFICE OF MANAGEMENTAND BUDGET, WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2) LER NUMBER (6) PAGE (3)
N SEOUENTIAL J~gP REVISION NUMSER vo< NUMSER Washin ton Nuclear Plant - Unit 2 0 5 0 0 0 3 9 7 9 0 0 0 OF TEXT /ifmore e/reoe le>>rloPed, rr>> eddlrlolre/NRC Form 3664'e/ (12)
- 4. Although there were no structures, components or systems inoperable prior to the event which contributed to the event, the equipment affected by this problem are SGT system filter trains SGT-FU-lA and SGT-FU-1B.
B. Further Corrective Action
- l. This situation was reviewed relative to the requirements of 10CFR50. 59 and it was determined that it represents an unreviewed safety question.
Accordingly, the NRC was formally notified of this determination.
- 2. To confirm that the aforementioned actual Secondary Containment leakage value has remainea representative of the Plant condition, a test was run on September 26, 1989. The leakage was found to be 1228 cfm; thus, con-firming the 1475 cfm value used for the JCO.
- 3. Design Basis changes will be evaluated to provide an SGT system that allows for adequate filtering of Secondary Containment for applicable meteorological conditions, and system draw down time, so as to meet 10CFR100 and GDC 19 limits, while taking credit for suppression pool scrubbing as allowed by SRP 6. 5. 5.
- 4. Current system testing will be maintained to ensure Secondary Containment leakage and SGT flow capabilities are within the JCO analysis.
- 5. The NNP-2 FSAR will be revised to show the correct X/(} values.
Safet Si nificance Given the current state of Secondary Containment integrity, the SGT can provide adequate differential pressure control with an adequate margin applied for variations in Secondary Containment leak-tightness and SGT flow performance. Based upon actual Plant conditions arid system performance, the Secondary Containment pressure differential will remain greater than -0.25H during severely cold winter conditions; with temperatures as low as -23/F without wind and -8/F with a coincident 10 mph wind. Although formal calculations have not been prepared, preliminary calculations show that both offsite post accident doses remain well below 10CFR100 limits and, with credit for suppression pool scrubbing, not significantly different than the results now documented in the FSAR.
NRC Form 366A (6JIB)
NRC FORM 366A (64)9)
LICENSEE EVE TEXT CONTINUATION V.S. NUCLEAR REGULATORY COMMISSION REPORT ILER) t APPROVED OMB NO. 31600104 E XPIR E S: 4/30/92 ESTIMATED BURDEN PER RESPONSE TO COMPLY WTH THIS INFORMATION COLLECTION REQUEST: 60A) HRS. FORWARD COMMENTS REGARDING BURDEN ESTIMATE TO THE RECORDS AND REPORTS MANAGEMENT BRANCH (P.530), U.S. NUCLEAR REGULATORY COMMISSION. WASHINGTON, DC 20555, AND TO 1HE PAPERWORK REDUCTION PROJECT (3(500104), OFFICE OF MANAGEMENTAND BUDGET,WASHINGTON, DC 20503.
FACILITY NAME (1) DOCKET NUMBER (2I- LER NUMBER (6) PAGE (3)
YEAR gj% SEQVE NTIAL >~~ REVISION NUMSER "<YA NUMBER Washin ton Nuclear Plant - Unit 2 o s o o o 39 90 0 0 01 8 o"0 8 TEXT /llmore SOece /4 ler)o/red. fee edde'one/ NRC Forrrr 3664'4/ ()7)
In light of the X/Q input errors discovered on January 8, 1990, the Unreviewed Safety Question Analysis originally prepared was reviewed and revised. Although the errors in FSAR methodology compound the offsite dose consequences, the study calculations performed to assess the impact of this discovery continue to support the conclusions of the original analysis. The conclusion remains that both the offsite and onsite post accident doses are within the 10CFR100 limits using the correct X/Q values in the atmospheric dispersion model.
Similar Events LER 88-023 EIIS Information Text Reference EIIS Reference System Component Standby Gas Treatment (SGT) System BM Secondary Containment NG Standby Service Water (SSW) BS Emergency Diesel Generator EK GEM Reactor Building Exhaust and Outside Air (REA and ROA) Isolation Valves VA ISV SGT-FU-lA and SGT-FU-1B BM FLT NRC Form 366A (64)9)