ML17266A252

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LER 80-033/03L-0:on 800724,while at 100% Power,Control Element Assembly 63 Dropped to Fully Inserted Position. Caused by Technician Accidently Shorting Output of 15-volt Power Supply While Taking Routine Voltage Measurements
ML17266A252
Person / Time
Site: Saint Lucie NextEra Energy icon.png
Issue date: 08/25/1980
From: Pace P
FLORIDA POWER & LIGHT CO.
To:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
Shared Package
ML17208A955 List:
References
LER-80-033-03L, LER-80-33-3L, NUDOCS 8009020372
Download: ML17266A252 (1)


Text

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of the 15 These measurements, intended to detect failin su lies before failure have been discontinued due to the close quarters and risk of shortin these supplies.

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