LER-1978-038, /01T-0 on 780925,input Error Made to ECCS Analysis Re Containment Spray Flow.Caused by Ambiguous Data Supplied by Ae.Amend to Cycle 2 ECCS Analysis Will Be Issued Shortly |
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| 3351978038R01 - NRC Website |
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analvsis it was determinded that 'an error had been made in the input L- 'o the St. Lucie ECCS anal sis concerning the containment spray flow rate.)
) The NSSS vendor erformed a reanalysis for Cycle 2 using the corrected spray pump flow.
The reanalysis on this item confirms that St. Lucie 1
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REPORTABLE OCCURRENCE 335-78-38 LICENSEE EVENT REPORT PAGE TWO ADDITIONAL EYENT DESCRIPTION During review of the ECCS parameters for the Cycle 3 reload safety analysis, it was determined that an error had been made in the input to the St. Lucie ECCS analysis concerning the containment spray flow rate.
The flow rate used was the value for I pump, not the required 2-pump flow rate.
To evaluate the impact of this error, an analysis was performed for Cycle 2 by the NSSS vendor usinp, the corrected spray pump flow.
- Lhereas, the prior ECCS analyses has used reflood heat transfer coefficients derived from COHPRERC-II based upon spray pump flow of 3375 gpm and a Peak Linear Heat Generation Rate (PLHGR) of l7.0 kw/ft, the new analysis used reflood heat transfer coefficients based on a spray pump flow of 6750 gpm and the current PLHGR Technical Specification limit of 14.8 kw/ft.
In each case the Peak Clad Temperature (PCT) was determined using STRIKIN-II with a
PLHGR of l4.8 kw/ft and the respective reflood heat transfer coeffici-ents.
The increase in reflood heat transfer coefficients resulting from thE. reduction in PLHGR from l7.0 to 14.8 kw/ft more than offset any decrease in heat transfer coefficients due to the doubling of spray pump flow.
As a result the PCT calculated by STRIKIN-II decreased from the value of 2035 F determined for Cycle 2 to a revised value of 2022 F.
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This completes the renalysis on this item and confirms that St.
Lucje does not exceed the Appendix K limit.
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| 05000250/LER-1978-017-03, /03L-0:on 780514,improper Switching at Pratt & Whitney Substation & Incorrect Wiring of Protective Relays at Midway Substation Led to de-energization.Offsite Power Lost.Incorrect Wiring Corrected | /03L-0:on 780514,improper Switching at Pratt & Whitney Substation & Incorrect Wiring of Protective Relays at Midway Substation Led to de-energization.Offsite Power Lost.Incorrect Wiring Corrected | | | 05000250/LER-1978-017, Forwards LER 78-017/03L-0 | Forwards LER 78-017/03L-0 | | | 05000335/LER-1978-025-03, /03L-0 Update on 780905:2 Damper Motors in Suction Line for HVE-9B Blew Fuses in Control Circuits, Causing B Train to Be Oper, Rather than Inoper as Previously Reported.Condition Is Not Reportable Per Tech Specs | /03L-0 Update on 780905:2 Damper Motors in Suction Line for HVE-9B Blew Fuses in Control Circuits, Causing B Train to Be Oper, Rather than Inoper as Previously Reported.Condition Is Not Reportable Per Tech Specs | | | 05000335/LER-1978-033-03, /03L-0 on 780901:During Plant Startup from Short Maint Shutdown, the Dose Equivalent of Iodine Exceeded Tech Spec Due to Plant Shutdown & Subsequent Startup Transients | /03L-0 on 780901:During Plant Startup from Short Maint Shutdown, the Dose Equivalent of Iodine Exceeded Tech Spec Due to Plant Shutdown & Subsequent Startup Transients | | | 05000335/LER-1978-033, Forwards LER 78-033/03L-0 | Forwards LER 78-033/03L-0 | | | 05000335/LER-1978-034-03, /03L-0 on 780902:during Short Maint Shutdown, Charging Pump 1A Was Found to Have Cracked Pump Casing, Probably Due to Suction cavitation.1Apump Casing Will Be Replaced & Damping Device Installed on Pump Suction Line | /03L-0 on 780902:during Short Maint Shutdown, Charging Pump 1A Was Found to Have Cracked Pump Casing, Probably Due to Suction cavitation.1Apump Casing Will Be Replaced & Damping Device Installed on Pump Suction Line | | | 05000335/LER-1978-034, Forwards LER 78-034/03L-0 | Forwards LER 78-034/03L-0 | | | 05000335/LER-1978-035-03, /03L-0 on 780905:During Full Pwr Oper 2 Damper Motors in the Suction Line for ECCS Area Exhaust Fan HVE-9B Blew Control Circuit Fuses,Caused by Loss of Insulating Fluid Thru Leaking Gasket in One Motor,Shorting Both Out | /03L-0 on 780905:During Full Pwr Oper 2 Damper Motors in the Suction Line for ECCS Area Exhaust Fan HVE-9B Blew Control Circuit Fuses,Caused by Loss of Insulating Fluid Thru Leaking Gasket in One Motor,Shorting Both Out | | | 05000335/LER-1978-035, Forwards LER 78-035/03L-0 | Forwards LER 78-035/03L-0 | | | 05000335/LER-1978-036-03, /03l-0 on 780905:during Monthly Surveillance on a Diesel Generator the 4160V Tie Breaker to Its Emergency Bus Would Not Close Remotely from Control Room Due to Dirty Contacts on Oper Relay | /03l-0 on 780905:during Monthly Surveillance on a Diesel Generator the 4160V Tie Breaker to Its Emergency Bus Would Not Close Remotely from Control Room Due to Dirty Contacts on Oper Relay | | | 05000335/LER-1978-036, Forwards LER 78-036/03l-0 | Forwards LER 78-036/03l-0 | | | 05000335/LER-1978-037, Forwards LER 78-037/01T-1 | Forwards LER 78-037/01T-1 | | | 05000335/LER-1978-037-01, /01T-1 on 780919:during Sys Insp,Class I Longitudinal Braces on Auxiliary Bldg Ventilation Ducts Were Found Missing.Caused by Unique Combination of Personnel Errors | /01T-1 on 780919:during Sys Insp,Class I Longitudinal Braces on Auxiliary Bldg Ventilation Ducts Were Found Missing.Caused by Unique Combination of Personnel Errors | | | 05000335/LER-1978-038-01, /01T-0 on 780925,input Error Made to ECCS Analysis Re Containment Spray Flow.Caused by Ambiguous Data Supplied by Ae.Amend to Cycle 2 ECCS Analysis Will Be Issued Shortly | /01T-0 on 780925,input Error Made to ECCS Analysis Re Containment Spray Flow.Caused by Ambiguous Data Supplied by Ae.Amend to Cycle 2 ECCS Analysis Will Be Issued Shortly | | | 05000335/LER-1978-038, Forwards LER 78-038/01T-0 | Forwards LER 78-038/01T-0 | | | 05000335/LER-1978-039-03, /03L-0:on 780930,during Power Operation,Digital Processing Sys Malfunctioned.Caused by Momentary Memory Failure.Sys Repaired & Placed Back in Svc in 70 Minutes | /03L-0:on 780930,during Power Operation,Digital Processing Sys Malfunctioned.Caused by Momentary Memory Failure.Sys Repaired & Placed Back in Svc in 70 Minutes | | | 05000335/LER-1978-039, Forwards LER 78-039/03L-0 | Forwards LER 78-039/03L-0 | | | 05000335/LER-1978-040, Forwards LER 78-040/03L-0 | Forwards LER 78-040/03L-0 | | | 05000335/LER-1978-040-03, /03L-0 on 781002:During Pwr oper,1B Charging Pump Failed to Start While Only 1C Pump Was operable.Cause:1B Suction Pressure Gage Waspegged Highdue to Leaking Valve. Valve Repaired,Gage Vented & Pump Returned to Svc | /03L-0 on 781002:During Pwr oper,1B Charging Pump Failed to Start While Only 1C Pump Was operable.Cause:1B Suction Pressure Gage Waspegged Highdue to Leaking Valve. Valve Repaired,Gage Vented & Pump Returned to Svc | | | 05000335/LER-1978-041, Forwards LER 78-041/01T-0 | Forwards LER 78-041/01T-0 | | | 05000335/LER-1978-041-01, /01T-0 on 781103:water from Reactor Coolant Sys Injected Through a Containment Spray Header.Caused by Improper Clearance Removal Instructions & 2 Isolation Valves Opened Between Spray Sys & Shutdown Cooling Sys by Operator | /01T-0 on 781103:water from Reactor Coolant Sys Injected Through a Containment Spray Header.Caused by Improper Clearance Removal Instructions & 2 Isolation Valves Opened Between Spray Sys & Shutdown Cooling Sys by Operator | | | 05000335/LER-1978-042-01, /01T-0 on 781111:4 Solenoid Operated Naoh Addition Sys Valves Found de-energized Due to Failure to Replace Fuses for Valves SE07-1A,1B,2A & 2B During Plant Heatup & Following Outage | /01T-0 on 781111:4 Solenoid Operated Naoh Addition Sys Valves Found de-energized Due to Failure to Replace Fuses for Valves SE07-1A,1B,2A & 2B During Plant Heatup & Following Outage | | | 05000335/LER-1978-042, Forwards LER 78-042/01T-0 | Forwards LER 78-042/01T-0 | | | 05000335/LER-1978-043-03, /03L-1 on 781120:during Power Operation Cambridge Electron Accelerator 62 Slipped 13 Inches a Second Time to Point 43 Inches Below Original Position.Personnel Misinterpreted Tech Specs | /03L-1 on 781120:during Power Operation Cambridge Electron Accelerator 62 Slipped 13 Inches a Second Time to Point 43 Inches Below Original Position.Personnel Misinterpreted Tech Specs | | | 05000335/LER-1978-043, Forwards LER 78-043/03L-0 | Forwards LER 78-043/03L-0 | | | 05000335/LER-1978-044, Forwards LER 78-044/03L-0 | Forwards LER 78-044/03L-0 | | | 05000335/LER-1978-044-03, /03L-0 on 781121:motor Operated Valve Mv 07-13 Failed to Open Electrically Following Closure Due to Faulty Torque Switch on Valve Operator.Switch Replaced & Valve Checked | /03L-0 on 781121:motor Operated Valve Mv 07-13 Failed to Open Electrically Following Closure Due to Faulty Torque Switch on Valve Operator.Switch Replaced & Valve Checked | | | 05000335/LER-1978-045-03, /03L-1 on 790305:during Power Operation,Digital Data Processing Sys Malfunctioned.Caused by Error in Program Installed by Licensee in June 1978.Program Error Corrected | /03L-1 on 790305:during Power Operation,Digital Data Processing Sys Malfunctioned.Caused by Error in Program Installed by Licensee in June 1978.Program Error Corrected | | | 05000335/LER-1978-045, Forwards LER 78-045/03L-1 | Forwards LER 78-045/03L-1 | | | 05000335/LER-1978-046-03, /03L-0 on 781207:during Power Operation,Control Element Assembly 59 Dropped as It Was Manually Inserted to 100 in Position for Moderator Temp Coefficient Test.Cause Unknown | /03L-0 on 781207:during Power Operation,Control Element Assembly 59 Dropped as It Was Manually Inserted to 100 in Position for Moderator Temp Coefficient Test.Cause Unknown | | | 05000335/LER-1978-046, Forwards LER 78-046/03L-0 | Forwards LER 78-046/03L-0 | | | 05000333/LER-1978-089, Forwards LER 78-089/03L-0 | Forwards LER 78-089/03L-0 | |
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