ML17265A171
| ML17265A171 | |
| Person / Time | |
|---|---|
| Site: | Ginna |
| Issue date: | 02/09/1998 |
| From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML17265A169 | List: |
| References | |
| 50-244-97-12, NUDOCS 9802200151 | |
| Download: ML17265A171 (57) | |
See also: IR 05000244/1997012
Text
. U.S. NUCLEAR REGULATORYCOMMISSION
REGION I
License No.
Report No.
50-244/97-1 2
I
Docket No.
50-244
Licensee:
Facility Name:
Location:
Rochester Gas and Electric Corporation (RGKE)
R. E. Ginna Nuclear Power Plant
'1503 Lake Road
Ontario, New York 14519
Inspection Period:
November 17, 1997 through January 4, 1998
Inspectors:
Approved by:
P. D. Drysdale, Senior Resident Inspector
C. C. Osterholtz, Resident Inspector
L. J. Prividy, Senior Reactor Engineer
P. R. Frechette, Physical Security Inspector
G. C. Smith, Senior Physical Security Inspector
J. C. Jang, Senior Radiation Specialist
D. M. Silk, Senior Emergency Preparation Specialist
L. T. Doerflain, Chief.
Projects Branch
1
Division of Reactor Projects
98022001.M
980209
ADOCK 05000244
8
EXECUTIVE SUMMARY
R. E. Ginna Nuclear Power Plant
NRC Inspection Report 50-244/97-12
This integrated inspection included aspects of licensee operations, engineering,
maintenance,
and plant support.
The report covers a 7-week period of resident inspection.
In addition, it includes the results of announced inspections by a regional security
specialist, and an engineering specialist.
~Oerations
The licensee's effort to reduce the number of operator workarounds and challenges during
the outage was successful.
The operator workaround program had been appropriately
implemented to identify plant deficiencies as workarounds or challenges.
The safety evaluation performed to bypass channel two average reactor coolant system
temperature
(Tave) from the rod control system was satisfactory.
The licensee's intention
to reconfigure the channel two temperature detectors during the next refueling outage was
considered appropriate.
Operator performance in response to the trip of both feedwater heater drain pumps was
good.
Improved technical specification (ITS) requirements were properly interpreted and
actions were taken in a timely manner.
The licensee considered that an instantaneous trip
signal was generated
by the heater drain tank low level switch, given that no abnormal
indications were observed
in pump performance throughout the rest of the'nspection
period.
Operators observed during a training scenario displayed a knowledge deficiency regarding
plant conditions that should automatically trip reactor coolant pumps (RCPs).
However,
the instructor identified the deficiency and conducted good on the spot remediation training
for correction.
The licensee effectively evaluated plant modifications for training needs.
The assigned
training methods for educating operations personnel appeared
appropriate.
Maintenance
Observed maintenance
and surveillance activities were performed in accordance with
procedural requirements.
Plant equipment received adequate post maintenance testing
prior to its return to service.
Good personnel and plant safety practices were observed.
With the exception of testing on the B-emergency diesel generator, the as-found and as-left
test data met the expected performance values and the specified acceptance
criteria stated
in the Updated Final Safety Analysis Report.
The licensee effectively identified and resolved problems with the hydrogen side seal oil
cooler.
The addition of a service water isolation valve for the cooler was considered
an
appropriate modification.
Executive Summary (cont'd)
Mechanical maintenance
personnel improperly entered out-of-specification test data into
two preventive maintenance
procedures for the 8-emergency diesel generator,
and certified
the data as satisfactory without consulting with maintenance management.
The failure to
comply with the administrative requirements of nuclear directive ND-MAI,administrative
procedure A-1603.5, and maintenance
procedure M-15.1M is a violation of 10 CFR 50,
Appendix 8, Criterion V (VIO 50-244/97-12-01).
~En ineerin
System engineering provided adequate technical support to resolve problems in the
auxiliary feedwater system.
The licensee's commitments made in the 10 CFR 50.54(f) response letters concerning
licensing and design basis'activities were being appropriately implemented.
Two EDG performance parameters that could impact engine operability were not
incorporated into the licensee's test procedures.
The need to incorporate additional
operability limits requires additional review. The inspectors willfurther evaluate the EDG's
critical performance parameters,
and the need to incorporate them into the licensee's test
procedures for operability considerations
(IFl 50-244/97-12-02).
Plant Su
ort
The licensee maintained an adequate security and safeguards
program.
The conduct of
security activities met licensee commitments and NRC requirements.
Security facilities and
equipment were well maintained and reliable.
Security procedures were being properly
implemented, security staff knowledge, performance and training were acceptable.
Security organization and administration, and quality assurance
programs were adequate to
ensure effective implementation of the program.
The lock and key program was reviewed
and determined to be implemented in accordance with the requirements of the Security
Plan.
TABLEOF CONTENTS
EXECUTIVE SUMMARY
~
II
TABLE OF CONTENTS
IV
I. Operations
01
02
05
08
Conduct of Operations ....... ~.............
~......
1
01.1
General Comments..................
1
01.2
Summary of Plant Status ... ~..... ~....................
1
Operational Status of Facilities and Equipment ....................
2
02:1
Operator Workarounds and Challenges ....................
2
02.2
Average Reactor Coolant System Temperature
(Tave) Swings.....
3
02.3
Simultaneous Trip of Both Feedwater Heater Drain Pumps ....... 4
Operator Training and Qualification ......
~ .. ~.........
~ .,......
5
05.1
Licensed Operator Simulator Training ...... ~..............
~ 5
05.2
Outage Modification Training....... ~......
~ ~...
~ ~......
~ 5
Miscellaneous Operations Issues
~ .. ~....... ~........ ~.... ~.... 6
08.1
(Closed) LER 97-002: Loss of 34.5 KV Offsite Power Circuit 751,
Due to External Cause, Results in Automatic Start of "B"
Emergency
Diesel Generator ....................
6
08.2
(Closed) LER 97-004: Radiation Monitor Alarm, Due to Higher than
Normal Radioactive Gas Concentration, Results in Containment
Ventilation Isolation......
~ . ~.......,.......'
~.........
6
08.3
(Closed) LER 97-005: Undetected Unblocking of Safety Injection
Actuation SignaI While at Low Pressure
Condition, Due to Faulty
Bistable, Resulted in Inadvertent Safety Injection Actuation Signal
. 6
08.4
(Open) LER 97-006: Verification of Boron Concentration Not
Performed Due to Misinterpretation of Event Sequence,
Resulted in
Condition Prohibited by Technical Specifications .........
~ ~... 7
08.5
(Open) LER 97-007: Reactor Trip Instrumentation Would Have
Been in a Condition Prohibited by Technical Specifications ..
~ ~... 7
I. Maintenance
I
M1
M2
M3
Conduct of Maintenance........... ~....... ~.......
M1.1
General Comments on Maintenance Activities..........
M1.2
General Comments on Surveillance Activities
Maintenance and Material Condition of Facilities and Equipment ..
M2.1
Main Turbine Hydrogen Side Seal Oil Cooler Repair
Maintenance Procedures
and Documentation
M3.1
Emergency Diesel Generator (EDG) Preventive Maintenance
Procedures
t
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
.8
8.8.8.9.9
10
10
III. Engineering........... ~...................
E1
Conduct of Engineering ~..............
E1.1
General Comments.............
E1.2
System Engineering
E1.3
Licensing and Design Basis Activities
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
12
12
12
12
14
IV
Table of Contents (cont'd)
E2
ES.
Engineering Support of Facilities and Equipment
~ '15
E2.1
Emergency Diesel Generator (EDG) Test Parameters
and
Acceptance Criteria ....... ~........... ~...... ~...... 15
Miscellaneous Engineering Issues
.. ~.........................
16
E8.1
(Closed) Violation 50-244/96-06-02: Inadequate Safety Evaluation
Regarding Stroke Time Change for MOV-4616 .. ~...........
16
E8.2
(Updated) Unresolved Item 50-244/96-06-04:
System Reliability Optimization Program (SWSROP) Issues ...... 17
E8.3
(Updated) Unresolved Item 50-244/97-201-02:Valve Testing
Issues Regarding Certain CCW and Sl valves ~.... ~.........
18
IV. Plant
RS
.. 19
.. 19
Miscellaneous RP&C Issues......................
~ .
R8.1
(Closed) IFI 50-244/97-06-03: Potential Signal Loss of
Meteorological Monitoring System ......... ~....
Miscellaneous
EP Issues .. ~......................
~
~
P8.1
(Closed) IFI 50-244/96-01-03: Call Out Drills.......
Conduct of Security and Safeguards Activities
S1.1
Security Program Review
Status of Security Facilities and Equipment.........
~
~ ..
S2.1
Review of Facilities and Equipment
Security and Safeguards
Procedures
and Documentation ...
S3.1
Program and Procedure.Implementation
Security and Safeguards Staff Knowledge and Performance
.
S4.1
Personnel Performance......... ~...........
~
Security and Safeguards Staff Training and Qualifications
S5.1
Training and Qualification (T&Q) Records Review
Security Organization and Administration ........ ~.....
S6.1
Management Support of Security...............
Quality Assurance in Security and Safeguards Activities
S7.1
Quality Assurance Effectiveness ..... '..
Miscellaneous Security and Safeguards
Issues
S8.1
(Closed) Violation E97-339: Failure to Maintain an Ade
Vehtcle Barrier ~.........................
the
~
~ 19
.. 20
.. 20
.. 20
20
.. 22
.. 22
.. 23
.. 23
.. 24
.. 24
~ . 24
.
~ 24
.. 25
.. 25
.. 26
.. 26
.. 27
PS
S1
S2
S3
S4
S5
~
~
~
~
~
~
~
~
S6
S7
~
~
~
~
~
~
~
quate
~
~
~
~ 27
S Up port
I
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~ I
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
~
V. Management Meetings........'..."............
X1
Exit Meeting Summary ...............
L2
Review of UFSAR Commitments ........
.. 28
.. 28
.. 28
ATTACHMENTS
Attachment
1 - Partial List of Persons Contacted
- Inspection Procedures
Used
- Items Opened, Closed, and Discussed
- List of Acronyms Used
Re ort Details
I. 0 erations
01
Conduct of
Operations'1.1
General Comments
Ins ection Procedure
The inspectors observed plant operations to verify that the facility was operated
safely and in accordance with licensee procedures
and regulatory requirements,
This review included tours of the accessible
areas of the facility, verification of
engineered safeguards feature (ESF) systems operability, verification of proper
control room and shift staffing, verification that the plant was operated in
conformance with the improved technical specifications (ITS) and appropriate action
statements for out-'of-service equipment were implemented, and verification that
logs and records accurately identified equipment status or deficiencies.
Operator
performance throughout the inspection period was good.
01.2
Summa
of Plant Status
The plant was nearing the end of a refueling outage and in MODE 4 at the beginning
of the inspection period.
MODE 3 was entered at 6:12 a.m. on November 17,-
1997, and the plant was heating up in preparation for a reactor startup.
During the
heatup, a steam leak occurred on the A-steam generator steam flowtransmitter.
Containment was temporarily evacuated,
and the leak was isolated'in approximately
25 minutes.
On November 18, 1997, the licensee discovered that significant erosion had
occurred in the main feedwater discharge valves.
The licensee subsequently
performed an engineering evaluation that determined the valves were still able to
perform a main feedwater isolation if required.
The licensee indicated that the
valves would be refurbished during the 1999 refueling outage.
MODE 2 was
entered at 3:43 a.m. on November 19, 1997, and the re'actor went critical at
7:10 a.m. the same day.
MODE 1 was entered at 6:24 a.m. on November 20, 1997. The turbine was
manually tripped on the initial attempt to bring it on line due to an inability to
maintain condenser vacuum.
A vacuum leak was subsequently discovered on
the A-condenser hotwell manway.
The leak was repaired and the turbine was
successfully placed on line at 3:28 p.m. the same day.
The plant attained
100 percent power at 6:16 p.m. on November 24, 1997.
The rod control system
was maintained in the manual mode until December 19, 1997, to prevent
inadvertent rod motion due to the effects of primary temperature streaming (see
section 02.3).
'Topical headings such as 01, M8, etc., are used in accordance with the NRC
standardized reactor inspection report outline.
Individual reports are not expected to
address
all outline topics.
On November 25, 1997, both feedwater heater drain pumps simultaneously tripped
(see section 02.3).
Reactor power was reduced below 50 percent due to axial flux
differential. The A-heater drain pump was restarted about five hours later.
The
B-heater drain pump was restarted on November 26, 1997, in conjunction with a
power increase.
The plant returned to 100 percent power at 8:00 a.m. that
morning (see section 02.3).
On November 28, 1997, the licensee made a four hour report in accordance with
10 CFR 50.72 after operations personnel discovere'd that the main turbine hydrogen
side seal oil cooler was leaking oil into the plant's cooling water discharge canal
(see section M2.1). The leak was isolated and repaired, and the cooler was
returned to service on December 18, 1997.
02
Operational Status'of Facilities and Equipment
02.1
0 erator Workarounds and Challen
es
a.
Ins ection Sco
e (71707)
>,,~ ~
T
The inspectors reviewed the status of operator workarounds and challenges before
and after the refueling outage.
b.
Observations and Findin s
Prior to the refueling outa ge the licensee had six operator workarounds and nineteen
operator challenges incorporated in their program. After the outage, the numbers
were reduced to two workarounds and fourteen challenges.
Among the
'orkarounds eliminated were drifting condenser vacuum indication (pressure
transmitter tubing replaced), unreliable core exit thermocouple indication (system
replaced), and unreliable recirculation flowfor the B-auxiliary feedwater pump
(controller replaced).
The two workarounds remaining after the outage were:
~
Auxiliary building service water (SW) isolation valves must be locally
throttled open when restoring SW isolation; and,
~
The A-condensate booster pump is not equipped with an undervoltage trip.
Following a loss of bus 12A, it would be necessary to trip the pump prior to
restoring the bus.
The licensee indicated that the remaining two workarounds were currently being
evaluated for resolution.
The inspectors were previously concerned that some plant equipment deficiencies
were not being fully evaluated for operator workarounds (see IR 50-244/97-06).
The inspectors sampled several control room deficiencies for inclusion into the
operator workaround program (such as the average temperature bypass discussed
in
section 02.2).
No instance was identified during the current inspection where a
plant deficiency had not been properly evaluated.
3
c.
Conclusions
The inspectors concluded that the licensee's effort to reduce the number of operator
workarounds and challenges during the outage was successful
~ The operator
workaround program had beeri appropriately implemented to identify plant
deficiencies as workarounds or challenges.
02.2
Avera
e Reactor Coolant S stem Tem erature
Tave Swin s
a.
Ins ection Sco
e (71707)
The inspectors reviewed the licensee's
response to noted spiking in channel two
Tave.
b.
Observations
and Findin s
Following the plant startup and attainment of 100% power on November 24, 1997,
control room operators noted spiking on temperature instrument Tl-402 (Tave
channel two), and on TI-406 (delta T channel two). Operations personnel
subsequently maintained the rod control system in the manual mode to prevent
inadvertent rod motion. This anomaly had occurred before (see IR 50-244/96-12),
but was not severe enough to prevent placing the rod control system in automatic.
The spiking appeared to be related to reactor core age and was agg'ravated by the
locations of the reactor coolant system (RCS) temperature detectors.
Both
resistance temperature detectors (RTDs) for channel two were installed in
approximately the same location in the A-RCS loop. The other three channels have
RTDs located on opposite sides of the RCS piping, so when RCS fluid temperature
variations occurred, they tended to average out.
The licensee performed a safety evaluation (SEV-1113) to bypass the channel two
Tave input from the rod control system.
Channel two can be bypassed from the rod
control system by placing Tave defeat switch (T-401A) in defeat.
The safety
evaluation concluded that it was acceptable to bypass channel two since the Tave
defeat switch would bypass the rod control system, but not channel two's input to
the reactor protection system.
The licensee also considered it more desirable to
have rod control maintained in automatic for a faster response to plant transients.
Channel two was bypassed
and the rod control system was returned to the
automatic mode on December 19, 1997.
The licensee indicated that the channel two RTDs would be reconfigured to be
consistent with the other channels during the 1999 refueling outage.
The licensee
also identified that the channel two bypass would be considered an "operator
challenge" in accordance with the operator workaround program.
Conclusions
The inspectors concluded that the safety evaluation performed to bypass channel
two Tave from the rod control system was satisfactory.
The licensee's intention to
reconfigure the channel two temperature detectors during the next refueling outage
was appropriate.
02.3
Simultaneous Tri of Both Feedwater Heater Drain Pum
s
80
Ins ection Sco
e (71707)
The inspectors reviewed the licensee's response to a simultaneous trip of both
feedwater heater drain pumps.
b.
Observations and Findin s
On November 25, 1997, both feedwater heater drain pumps inexplicably tripped
with the plant at 100 percent power.
Control room operators reduced reactor
power to less than 90 percent within ten minutes.
However, reactor core axial flux
"penalty minutes" were being accrued in accordance with ITS 3.2.2, "Nuclear
Enthalpy Rise Hot Channel Factor," because
preconditioning requirements for
control rods restricted their being withdrawn more than three steps per hour.
Operations personnel reduced reactor power to less than 50 percent in accordance
with ITS 3.2.2. A total of 90 penalty minutes were accumulated.
The licensee
generated
an ACTION Report (97-2053) to address the heater drain pump trips, and
maintained plant power below 50 percent for 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> to eliminate the accrued
axial flux penalty minutes (ITS 3.2.2 prohibits operation above 50 percent until less
than 60 penalty minutes have been accrued during the previous 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />)
~
Troubleshooting activities revealed no obvious cause for the heater drain pump
trips. However, instrumentation and control (l&C) personnel considered that a
heater drain tank low level trip signal may have been inadvertently actuated by plant
personnel while moving heavy equipment in the vicinityof the pumps at the time.
The trip was activated by a mercury switch that could have instantaneously
generated
a trip signal if "bumped" or vibrated.
IKC personnel inspected the switch
and adjusted its alignment to increase the angle in which the switch sits to minimize
the possibility of inadvertent actuation.
The A-heater drain pump was restarted on
November 25, 1997, with test equipment installed and no abnormalities were
noted.
Both heater drain pumps were returned to service on November 26, 1997,
when the plant was returned to 100% power. The heater drain pumps ran normally
throughout the rest of the inspection period.
C.
Conclusions
The inspectors concluded that operator performance in response to the heater drain
pump trips was good.
ITS requirements were properly interpreted and actions were
taken in a timely manner.
The licensee's suspicion that an instantaneous trip signal
was generated
by the heater drain tank-low level switch appeared
likely, given that
no abnormal indications were observed
in pump performance throughout the rest of
the inspection period.
05
Operator Training and Qualification
~
~
05.1
Licensed 0 erator Simulator Trainin
80
Ins ection Sco
e (71707)
1
I,
The ins'pec'tors observed-aisimulator training scenario for licensed operators.
b.
Observations
and Findin s.
The inspectors observed
a simulator training scenario for licensed operators
conducted on December 19, 1997. The scenario included a degradation of offsite
power such that an underfrequency condition caused an automatic reactor trip.
'his
underfrequency condition should also automatically trip the reactor coolant
pumps (RCPs).. However, this automatic trip failed to actuate and the RCPs
remained running. The operating crew did not identify that the RCPs should be
tripped.
The instructor stopped the scenario and provided remedial training for the
operating crew on expected conditions for degraded grid frequency.
The scenario
was then restarted and the operating crew successfully mitigated the casualty.
Conclusions
The inspectors concluded that the observed crew displayed a knowledge deficiency
regarding plant conditions that should automatically trip RCPs.
However, the
instructor identified the deficiency and conducted good on the spot remediation
training for correction.
05.2
Outa
e Modification Trainin
a.
Ins ection Sco
e (71707)
The inspectors reviewed the licensee's training methods for plant modifications
installed during the refueling outage.
b.
Observations and Findin s
All plant modifications that were installed during the refueling outage were reviewed
by a licensed operator curriculum committee to evaluate the training needs. 'The
committee consisted of the operations manager, one licensed operator from each
shift, and one representative from training. Classroom training was conducted on
significant modifications, such as the reactor protection system channel ¹2
resistance temperature detector (RTD) module replacement, while simulator training
was conducted for modifications that directly impacted licensed operator duties,
such as the core exit thermocouple panel replacement
(see IR 50-244197-11).
Other training methods for less significant modifications included control room
required reading letters, notification letters, and shop briefings.
In all, training was
conducted on eighteen modifications for operations personnel.
~
C.
Conclusions
08
\\
The inspectors concluded that the licensee effectively evaluated plant modifications
for training needs.
The assigned training methods for educating operations
personnel appeared
appropriate.
T
'
Miscellaneous Operations Issues,
't
08.1
Closed
LER 97-002: Loss of 34.5 KV Offsite Power Circuit 751
Due to External
Cause
Results in Automatic Start of "B" Emer enc
Diesel Generator
082
LER 97-002 was submitted to the NRC on August 19, 1997, after the B'-EDG
automatically started. following a loss of offsite power circuit 751. The loss
occurred when a raccoon climbed a power distribution pole and caused
a short
circuit (see IR 50-244/97-06). The LER noted that the plant operated
as designed,
and that offsite circuit 751 was returned to.service when its protective relays were
reset.
The inspectors concluded that:the LER adequately described the event, and
appropriately addressed
the root causes
and corrective actions.
This LER is closed
(LER 97-002).
Closed
LER 97-004: Radiation Monitor Alarm Due to Hi her than Normal
Radioactive Gas Concentration
Results in Containment Ventilation Isolation
LER 97-004 was submitted to the NRC on November 24, 1997, after an automatic
isolation of containment ventilation occurred during removal of steam generator
inserts (see IR 50-244/97-11). The LER noted that the containment radiation
monitor alarm setpoint was only about one percent of the ITS limit, and that
radiation levels were slightly escalated
in containment due to the presence of a
defective fuel assembly.
The LER indicated that future refueling outage preparation
activities would specifically review the 'potential need to revise radiation monitor
setpoints based on RCS activity. The inspectors concluded that the LER adequately
described the event, and appropriately addressed
the root causes
and corrective
actions.
This LER is closed (LER 97-004).
08.3
Closed
LER 97-005: Undetected Unblockin
of Safet
In'ection Actuation Si nal
While at Low Pressure Condition
Due to Fault
Bistable
Resulted in Inadvertent
Safet
In ection Actuation Si nal
LER 97-005 was submitted to the NRC on December 1, 1997, after an inadvertent
automatic safety injection actuation signal was generated while performing a plant
safeguards
logic test (see IR 50-244/97-11). The B-EDG and two service water
pumps started, as designed; there was no actual injection as the rest of the systems
were out of service for the outage.
The LER indicated that the signal was generated
by a failed pressurizer pressure bistable.
The bistable was replaced arid calibrated,
08.4
and the logic tests were successfully completed.
The inspectors concluded that the
LER adequately described the event, and appropriately addressed
the root causes
and corrective actions.
This LER is closed (LER 97-005).
0 en
LER 97-006: Verification of Boron Concentration Not Performed Due to
Misinter retation of Event Se
uence
Resulted in Condition Prohibited b
Technical
LER 97-006 was submitted to the NRC on December 3, 1997, after the licensee
discovered that an ITS requirement to verify boron concentration following an
inoperability of the source range audible count rate may not have been performed
within the four hour time requirement.
The LER indicated that operations and
maintenance
procedures were inadequate
in assuring the operability of the audible
count rate. monitor.and would be reviewed and changed to ensure operability during
calibration and while in MODE 6. The LER also noted that there were no opera'tional
or safety consequences
attributed to the delayed boron concentration verification
since no core alterations or reactivity additions occurred while the audible count rate
was inoperable.
However, after issuing the LER, the licensee determined that
control room operators did not declare the audible count rate instrument inoperable
at the proper time, and that a revision to the LER would be necessary to identify
additional operator training in this area as a further corrective action.
This LER will
remain open pending a revision by the licensee and subsequent
NRC review (LER
97-006).
08.5
0 en
LER 97-007: Reactor Tri
Instrumentation Would Have Been in a Condition
Prohibited b
Technical S ecifications
LER 97-007 was submitted to the NRC on December 17, 1997, after the licensee
discovered that there was no requirement in instrumentation and control procedures
to place the neutron flux low range trip circuitry in the tripped condition for a power
range channel removed from service for physics testing in MODE 2 as required by
the ITS. The licensee made the discovery while in MODE 3, and thus prevented any
ITS discrepancy.
In addition, the licensee determined that a similar problem with
the high range trip circuitry occurred iri 1988, but was not reported to the NRC in
accordance with 10 CFR 50.73. That condition was corrected at the time;
however, that instance was also reported in this LER. The LER concluded, that the
uniqueness of the original design for placing neutron flux trip circuitry into a tripped
condition had not been emphasized
in procedures.
The LER indicated'that
instrumentation procedures would be revised and that training would be conducted
to ensure the neutron flux low range trip circuitry would be placed in the tripped
condition when required by the ITS. The licensee indicated that a revision to the
LER was necessary to correct a typographical error, and to identify additional
corrective actions to improve the documentation of specific instrument functions
that become inoperable when a channel is removed from service.
This LER will
remain open pending the licensee's revision and subsequent
NRC review
(LER 97-007).
If. Maintenance
M1
Conduct of Maintenance
h
M1.1
General Comments on Maintenance Activities
a.
Ins ection Sco
e 62707
The inspectors observed portions of plant maintenance activities to verify that the
'orrect parts and tools were utilized, the applicable industry codes and technical
specification,requiremen'ts
were satisfied, adequate
measures
were in place to
ensure personnel safety and prevent damage to plant structures, systems,
and
components,
and tb ensure that equipment operability was verified upon completion
of post maintenance testing.
b.
Observations and Findin s
The inspectors. observed all or portions of the following work activities:
~
Main turbine hydrogen seal oil'cooler reinstallation; observed on
December 17-18, 1997 (see section M2.1).
~
B-AFW pump recirculation flow controller replacement and pbst maintenance
testing; observed on December 29-30, 1997.
c.
Conclusions
a
The-inspectors concluded that the observed maintenance activities were performed
in accordance with procedural requirements.
Equipment received adequate
post-
maintenance testing prior to its return to service.
Good personnel and plant safety
practices were observed during the maintenance work.
M1.2
General Comments on Surveillance Activities
a.
Ins ection Sco
e 61726
'he inspectors observed one surveillance test to verify that an approved procedure
was in use, procedure details were adequate, test instrumentation was properly
calibrated and used, technical specifications were satisfied, testing was performed
by knowledgeable personnel, and test results satisfied acceptance
criteria or were
properly dispositioned.
9
b.
Observations
and Findin s
The inspectors observed portions of the following surveillance activity:
~
PT-16Q-B, "AFW Pump B - Quarterly;" observed on December 30,
1997
c.
Conclusions
The inspectors'confirmed that the procedure used was current and properly
followed. The shift supervisor properly authorized the surveillance work to proceed.
The licensee confirmed the qualifications of all surveillance test personnel involved
in the test.. The as-'found and as-left test data met the expected performance values
and the specified acceptance
criteria stated in the Updated Final Safety Analysis
Report.
M2
IVlaintenance and Material Condition of Facilities and Equipment
M2.1
Main Turbine H dro en Side Seal Oil Cooler Re air
a.
Ins ection Sco
e (62707)
The inspectors reviewed the licensee's response to a leak in the main turbine
hydrogen side seal oil cooler.
b.
Observations and Findin s
On November 28, 1997, the licensee discovered that the hydrogen side seal oil
cooler had developed
a leak. Security personnel noticed what appeared to be oil in
the low flow regions of the plant's cooling water discharge canal.
Operations
personnel subsequently discovered the leak and isolated'the cooler.
The licensee
generated
an ACTION Report (97-2064) to address the issue.
The licensee also
reported this event in accordance with'10 CFR 50.72 section b.2.vi. The cooler
was sent off site to a contractor facility.for repair, and it was discovered that a tube
to tubesheet joint leak had developed inside the cooler.
During the time the
hydrogen side seal oil cooler was isolated and removed, the air side seal oil cooler
provided oil flowto the hydrogen side.
After the cooler was repaired, it was reinstalled on December 17-18, 1997. A
service water isolation Valve for the cooler was also installed so the cooler could be
isolated without the use of blank flanges.
The cooler was returned to service on
'ecember
18, 1997.
10
The inspectors concluded that the licensee effectively identified and resolved
problems with the main turbine hydrogen side seal oil cooler.
The addition of a
service water isolation valve for the cooler was an appropriate modification.
M3
Maintenance Procedures
and Documentation
M3.1
Emer enc
Diesel Generator
EDG Preventive, Maintenance Procedures
a.
Ins ection Sco
e
(62707)'he
inspectors reviewed two work packages
used for the annual preventive
maintenance
on the A- and 8-EDGs that was accomplished during the recent 1997
refueling outage.
b.
Observations and Findin s
I
After the recent 1997 refueling outage; the inspectors reviewed outage work order
packages ¹19603808and ¹19603809,which were used for preventive
maintenance
on the A- and 8-EDGs.
The inspector's review followed the final
approval by maintenance supervision and their verification that all work specified in
the packages was completed satisfactorily.
Each package contained an official
record copy of procedure M-15.1M, ".A or 8 Diesel Generator Mechanical Inspection
and Maintenance."
This procedure provided detailed instructions for preventive
maintenance
on several diesel sub-systems
such as cooling water, fuel oil,
lubricating oil, and compressed
air; as well as inspections of engine components
such as the crankshaft, cylinder heads, valves, etc.
Following the mechanical
inspections, the procedure directed post-maintenance
and pre-operational testing to
verify that all maintenance was satisfactory before returning each EDG to service.
Step 5.20.1 of M-15.1M required technicians to record the firing temperature
and
pressure for each cylinder while the en'gine was operated and after it reached "full
load." The procedure also required that technicians record the difference between
the highest and lowest firing pressures
and clearly specified an acceptance
criteria
that this difference not exceed 150 psi maximum.
On November 4, 1997, cylinder
firing pressures
were taken during the performance of periodic test PT-12.2,
"Emergency Diesel Generator B." However, the actual difference between the
highest and lowest engine firing pressure was 160 psi, which the technicians
recorded and verified as acceptable.
All engine performance data in M-15.1M,
including the out-of-specification firing pressures,
was signed off by the technician
who took the data, and was also accepted
as satisfactory by a mechanic foreman.
Contrary to a note in procedure M-15.1M, the technicians recorded the out-of-
specification data as acceptable without contacting the appropriate maintenance
manager.
I
'11
The inspector also reviewed engine data taken during a previous refueling outage
when the B-EDG firing pressures
were obtained on May 3, 1996, using procedure
M-15.1M. During that test, the difference between the highest and lowest firing
pressure was recorded as 170 psi and signed off as satisfactory by the individual
taking the data, and also by a mechanic foreman.
The inspector further noted
several other recent instances during routine diesel diagnostic testing where this
parameter exceeded
150 psi on both the A- and B-EDG engines.
The inspectors discussed the out-of-specification data with the EDG system
engineer, who stated that the 160 psi pressure differential was primarily a concern
for engine balance and did not represent an operability limit. He also indicated that
'he out-of-specification data was discussed with the maintenance technicians during
the test.
However, neither the maintenance technicians or the system engineer
initiated an ACTION Report to address the discrepancy,
and a formal engineering
evaluation was not documented for the acceptability of the data.
The inspectors reviewed the licensee's administrative requirements pertaining to
procedure adherence.
Nuclear Directive ND-MAI,"Maintenance," established.
requirements for the execution of the licensee's maintenance
program, and assigned
responsibilities for program implementation.
ND-MAIcontained requirements to
document unexpected problems, and to refer any deficiencies to appropriate
supervision for resolution and disposition.
The directive also required that
deficiencies be reported in accordance with the licensee's
Correctiv'e Action
Program.
Administrative procedure A-1603.5, "Work Order Execution," specified
requirements for maintenance technicians to perform'procedures
as required and to
contact the appropriate maintenance
manager when unexpected conditions were
encountered.
Administrative procedure A-503, "Procedure Adherence
Requirements," contained requirements for the proper use of and adherence to plant
procedures.
However, this procedure appeared to contain a weakness,
in that no
specific instructions were provided to require that procedures
be adhered to as
written, and provided no other guidance to technicians on how to document out-of-
specification test data, or how to document the basis for the acceptability of out-of-
specification data prior to returning safety-related equipment to service.
The inspector discussed the out-of-specification data with the cognizant design
representative
(Fairbanks Morse) for the EDGs, who indicated that 10 to 20 psi
above the limitspecified in the vendor's technical manual did not represent
a
serious operating condition or an operability limitfor the engines (see section E2.1).
Nevertheless,
the inspectors were concerned that on two separate
occasions
maintenance technicians and foremen recorded out-of-specification test data in a
maintenance
procedure for safety-related equipment, and certified the data as
acceptable without contacting maintenance management
as required by procedures
ND-MAIand A-1603.5, and without resolving the discrepancy through the
Corrective'Action Program prior to returning the B-EDG to service.
~
'
'12
c.
Conclusions
The inspectors concluded overall that the annual preventive maintenance
on the A-
and B-EDGs was performed satisfactorily.
However, the licensee did not properly
adhere to the administrative requirements of procedures
ND-MAIand A-1603.5 to
properly comply with all procedure instructions, to resolve maintenance
discrepancies
through the Corrective Action Program, and to consult with
maintenance management when unexpected conditions are encountered
are a
violation of 10 CFR 50, Appendix B, Criterion V, "Instructions, Procedures,
and
Drawings" (VIO 50-244/97-12-01).
In addition, administrative procedure A-503
was weak in that it did not clearly delineate management expectations for the
appropriate actions by maintenance technicians when out-of-specification data is
obtained that is contrary to procedure requirements.
E1
Conduct of Engineering
E1.1
General Comments
Ins ection Procedure
'The inspectors reviewed engineering 'areas that included 1) the activities of the
engineering and technical support groups, including the role of the system engineer
in monitoring system performance and taking corrective actions for improvements;
2) the licensing and design basis activities associated with Rochester Gas and.
Electric's (RGS.E) commitments made in response to the NRC 10 CFR 50.54(f)
letter; and 3) RGRE's corrective actions regarding open items from a previous
engineering inspection (IR 50-244/96-06) and the Ginna plant design inspection
performed earlier in 1997.
E1.2
S stem En ineerin
80
Ins ection Sco
e (37550)
The inspector reviewed the preferred auxiliary feedwater (AFW) system and the
standby auxiliary feedwater system (SAFW) by conducting system walkdowns and
discussing with the system engineer the most recent system performance report,
and his involvement with several ACTION Reports for resolving equipment
problems.
t
Observations
and Findin s
The system engineer, who is responsible for the AFW and SAFW systems,
is also
assigned responsibility for the containment spray and spent fuel pool cooling
systems.
He had been assigned these responsibilities within the past year and was
familiar with the various procedures
required to perform these responsibilities.
The
inspector observed that the system engineer was aware of plant change request
(PCR)97-061 performed during the last refueling outage to improve the AFW
system design concerning two relays that were powered from a non-safety bus for
automatic starting of the three AFW pumps on a steam generator lo-lo level signal.
This system enhancement
was identified in the Ginna plant probabilistic safety
assessment
(PSA). The relays are now powered from a safety-related instrument
bus.
Although prior to implementation of PCR 97-061 the steam generator (SG) water
level lo-lo channels had been powered from nonsafety-related
Bus D, Technical
Specifications (TS) acknowledged this design feature and required that this logic
train be declared inoperable (per TS 3.3.2) if Bus D were unavailable.
However,
from a safety perspective, other means*existed at Ginna to automatically start the
AFW pumps, such as opening of the main feedwater pump breakers (which would
be a consequence
of the loss of offsite power), or a safety injection actuation
signal.
Also, AFW makeup and cooling to the SG's is not required for the first
10 minutes of a design basis event, allowing time for manual action if needed.
Therefore while significant with respect to being a primary actuation signal the
total.loss of actuation signal was considered to be a very low probability event.
Regarding the performance of major equipment in the AFW system, the system
engineer interacted well with the testing personnel who perform and oversee the
inservice testing of pumps, valves, and heat exchangers.
For example, the system
engineer was adequately following a potential backleakage
problem with SAFW
system check valves (9704B, 9705B) associated with the D-SAFW Pump.
Also,
the system engineer was closely following actions needed to resolve operational
problems with the B-AFW pump recirculation flow valve (4310) which was
identified as one of the plant "Operator Workarounds."
However, the inspector
noted that the deficiency identified in the existing ACTION Report (AR) 97-1117
was a repeat occurrence similar to two previous failures (ARs 97-0153 and
97-0635) concerning this valve which was an indication of past ineffective
corrective actions.
During discussions related to system engineer training and the planning and
prioritization of work, it was apparent that the AFW system engineer recognized the
need to learn more detail regarding his systems while also trying to perform other
tasks assigned,
such as the UFSAR verification and design basis documentation
projects (see section E1.2).
~ ~
'14
Conclusions
System engineering was providing adequate technical support in taking corrective
actions to resolve problems in the AFW system.
Licensin
and Desi
n Basis Activities
Ins ection Sco
e (37550)
The inspector reviewed the status of the*licensing and design basis activities
committed to in RG&E's response of February 7,1997, to the NRC request for
information pursuant to 10 CFR 50.54(f),
~
Observations
and Findin s
RG&E updated their 50.54(f) response
in a letter dated September 30, 1997,
wherein they indicated that the UFSAR,verification project would be completed by
October 1998 and then followed by the design basis documentation
(DBD) project
to be completed in December 2001. The licensee planned to utilize the system
engineers for the detailed reviews needed for these projects, thereby retaining the
knowledge and insights from their reviews and better equipping them for their daily
work. The DBD project is to include all high and medium risk significant systems
which actually totaled 16 systems compared to 14 systems mentiohed in RG&E's
February 7, 1997, response letter. The licensee indicated that some low risk-
significant systems, such as the AFW system, may also be included in the DBD
project.
The inspector noted that several UFSAR verification project guidance documents
had been issued by the project coordinator: 1) "UFSAR Verification Project
Administiative Guideline;" 2) "UFSAR Verification Deviation Processing Guideline;"
and 3) "UFSAR Verification Review Process
and Computerized Database
Guideline."
While the system engineers had been trained on the Use of these documents to
perform system reviews, the computerized database to collect the changes from the
reviews was not yet operational.
A line-by-line review of the UFSAR was planned.
Such a review had been done for the AFW and safety injection (Sl) systems, but all
comments and changes were still in hard-copy format. The UFSAR verification
project was scheduled to proceed in parallel with the, validation of all other design
basis source documents so that an electronic link of these source documents to a
living UFSAR could be accomplished by October 1998 for use during the DBD
project.
With their completion of the service water safety system functional inspection
(SSFl) and the NRC design team inspection of Ginna, RG&E noted in the updated
response letter of September 30, 1997, that they had completed the commitment to
perform two SSFls in 1997.
RG&E indicated that they would perform a SSFI of the
AFW system in 1998.
c.
Conclusions
"15
RG&E was adequately implementing commitments made in the 10 CFR 50.54(f)
response letters concerning licensing and design basis activities.
E2
Engineering Support of Facilities and Equipment
E2.1
Emer enc
Diesel Generator
EDG Test Parameters
and Acce tance Criteria
a 0
Ins ection Sco
e (37551)
b.
The inspector reviewed maintenance
and test procedures used by the licensee to
perform post-maintenance
and ITS surveillance testing of the EDGs.
Observations
and Findin s
Periodic test procedures PT-12.1, "Emergency Diesel Generator A," and PT-12.2
"Emergency Diesel Generator B," contained the principal tests used to demonstrate
operability of both EDGs.~ These procedures were normally used for the monthly
surveillance test of each diesel as required by ITS section 3.8.1, but they are also
performed following significant maintenance when an operational performance test
is required to restore the diesel to service.
The test acceptance
criteria relating to
engine operability included critical performance parameters
such as total power
output, engine exhaust temperatures,
generator voltage and frequency, automatic
alignment to its associated
safeguards
bus, etc.
PT-12.1 and PT-12.2 were both
performed at 2000 + 50, -0 kilowatts (KW) to ensure that the operability tests are
performed above the upper band of the continuous rating defined in the ITS (1950
%50 KW).
The criterion for a maximum 150 ps'i differential between the highest and lowest
peak firing pressure was contained in the maintenance instructions of the EDG
vendor's technical manual (VTD-A0152-4004), and was specified as a limitthat is
applicable to the engine at full rated load (1950 KW). Maintenance procedures
M-15.1M, "A or B Diesel Generator Mechanical Inspection and Maintenance," also
defined EDG "fullload" as 1950 a50 KW. Since the engine firing pressures
recorded in procedure M-15.1M were specified for the engine's full load, the
acceptance
criteria did not match the test conditions required for PT-12.1 and
PT-12.2. The licensee acknowledged that the acceptance
criteria were
not'ppropriate
for the test conditions and subsequently initiated a procedure change
notice (PCN 97-2874) to delete the firing pressure data from procedure M-15.1M.
The inspectors contacted the diesel vendor/design representative
(Fairbanks Morse)
who stated that owner's of these'engines
should take corrective actions when the
- difference between the highest and lowest firing pressures
exceeded 200 psi.
However, the licensee did not have any procedure or test restrictions on operation
above a 200 psi differential, and data from recent engine diagnostic tests indicated
that value had been exceeded
on several occasions.
The design representative
also
stated that the maximum peak firing pressure for these engines shouldnever exceed
I
e
I
'16
2000 psig under any circumstances.
The licensee was unable to identify any
vendor document where this specification was stated; however, based upon the
design representative's
statement, the inspector considered that this value could
represent an operability limitthat was not recognized in the licensee's procedures,
and that no instructions to operators or test personnel were provided to avoid
exceeding that value.
The licensee indicated that peak firing pressures
in excess of
1900 psig have been observed on some cylinders during tests at high loads.
The
instrument gage used by the licensee to record this parameter was not part of a
calibration program.
Since the gage was not calibrated, the licensee could not
confirm that any cylinder had not exceeded
a firing pressure of 2000 psig; however,
there had not'been any signs of engine damage from the results of preventive
maintenance
inspections and diagnostic tests performed in recent years.
C.
Conclusions
ES.
The inspectors concluded that the appropriate acceptance
criteria for two EDGE
performance parameters that could impact engine operability were not incorporated
into the licensee's test procedures.
The inspectors could not determine if the limits
of the unmonitored parameter limits had been exceeded;
however, the need to
incorporate additional operability limits requires additional review. The inspectors
willfurther evaluate the EDGE's critical performance parameters,
and the need to
incorporate them into the licensee's test procedures for operability considerations.
Therefore, this will remain an inspector follow-up item (IFI 50-244/97-12-02).
Misceifaneovs Engineering Issues
E8.1
Closed
Violation 50-244 96-06-02: Inade uate Safet
Evaluation Re ardin
Stroke
Time Chan
e for MOV-4616
This violation was issued because the licensee had not adequately evaluated the
safety impact of the stroke time change for the auxiliary building service water
isolation valve (MOV-4616). Specifically, the valve had'been modified such that its
original stroke time of approximately 30 seconds was changed to approximately
120 seconds without fully evaluating the effects of this change on the performance
of the service water system to function under design basis conditions.
Corrective
actions included: 1) revising procedures
IP-SEV-1, "Preparation, Review, and
Approval of Safety Reviews," and IP-SEV-2, "Preparation, Review, and Approval of
Safety Evaluations;" 2) training plant personnel regarding the revised procedures
and the need to perform an increased scope of evaluation, especially when the plant
changes involve a safety related system and are beyond the level of detail of the
UFSAR; 3) restoring the valve stroke time to 30 seconds during the 1997 refueling
outage; and 4) in the longer term, compiling a controlled document available to plant
personnel to explicitly document all variables (stroke time, flow rate, etc.) that are
assumed
in the Accident Analysis chapter of the UFSAR.
The inspector verified that the revisions to procedures
IP-SEV-1 and IP-SEV-2 had
been issued and that appropriate training of plant personnel regarding these
procedures
had been conducted.
The inspector also verified that PCR 95-096,
'17
Revision 1, had been implemented in November 1996 to restore the MOV-4616
stroke time to approximately 30 seconds.
The actual valve stroke time recorded
during the post modification test procedure PT-2.3, "Safeguard Motor Operated
Valve Operation," was between 29 and 30 seconds.
The inspector noted that the
licensee work in compiling a document of all variables used in the UFSAR Accident
Analysis chapter was partially'complete and was scheduled for completion by
March 1, 1998, according to Item O'R05598in the licensee's Commitment and
Action Tracking System (CATS). Based on these actions, this item is closed.
U dated
Unresolved Item 50-244 96-06-04: Service Water S stem Reliabilit
0 timization Pro ram
SWSROP
Issues
This item was opened to identify the need for follow-up inspection in several areas:
1) the SWSROP should be revised to reflect the current SW system configuration;
2) the licensee had not fullyevaluated the 1993, 1994, and 1995 data regarding
heat exchanger performance tests; 3) several licensee-identified errors in the 1993
and 1994 component cooling water (CCW) heat exchanger test reports regarding
the effect of plugged tubes had not been corrected; and 4) the licensee's
CCW heat
exchanger performance calculations had,not-accounted
for possible macrofouling in
the SW side of the heat exchanger.
'
The licensee developed the SWSROP as an engineered
program largely in response
to the concerns identified in Generic Letter (GL) 89-13, "Service Water System
Problems Affecting Safety-Related Equipment."
Some of the folloW-up areas in this
open item, such as the need to update the SWSROP, had been noted during a
December 1994 self-assessment
that was performed to determine the status of
actions taken to resolve the, open items from a 1991 NRC Service Water System
Operational Performance Inspection.
As noted in Inspection Report (IR)
50-244/96-06,the
licensee had performed poorly in addressing the many open
items identified during the December 1994 self-assessment,
with the major
technical issues being related to heat exchanger performance testing.
In response to the NRC request included in IR 50-244/96-06regarding
specific plans
to complete the initial GL 89-13 service water heat exchanger thermal performance
test program, the licensee submitted on January 31, 1997, their plans for
completing this test program. After completing the review and evaluation of all
prior test data that spanned from 1992 to 1996, the licensee considered it
necessary to perform additional performance tests in 1997 on the standby AFW
pump room coolers, the containment recirculating fan coolers (CRFC), the CRFC
motor coolers, the diesel generator jacket water heat exchangers
and lube oil
coolers, and the CCW heat exchangers.
The initial test program for the spent fuel
pool heat exchanger was considered to be complete.
The inspector considered that
the licensee was appropriately evaluating the 1997 thermal performance data for
the-aforementioned
heat exchangers to establish test and/or cleaning frequencies
for inclusion into the preventive maintenance
(PM) systems.
However, establishment of PM frequencies was not yet complete for several
reasons.
For example, the licensee considered that another thermal performance
I
'18
test willbe warranted for the CCW heat exchangers
during the 1999 refueling
outage.
After review of the 1997 CCW heat exchanger test data, the licensee
noted that the A-CCW heat exchanger had a much higher tube fouling than the "B"
CCW heat exchanger.
It appeared that the B-CCW heat exchanger was receiving
more service water flowthan the A-CCW heat exchanger.
The licensee issued
ACTION Report 97-2149 (Dec'ember 12, 1997) to confirm this assumption and to
evaluate this variation in fouling'for its impact on the capability of the A-CCW heat
exchanger.
The licensee noted, and the inspector agreed, that immediate
operability was not a concern since both CCW heat exchangers
were cleaned after
the testing, and the service water temperature at this time was well below the
design basis limitof 80'F.
The licensee sponsored
a safety system functional inspection (SSFI) of the SW
system from March 31 to May 15, 1997 which was performed by an independent
contractor (Sargent and Lundy):. This SSFI resulted in about a 100 new action items
added to the licensee's CATS. In addition to issues related to heat exchanger
performance testing and revision of the SWSROP, comments were made regarding
the need to update'the SW system hydraulic flow model since it under predicted
flows in some cases.
= The licensee indicated that this work was being done in-
house and was scheduled for completion by the end of January 1998.
.This item willremain open pending:
1) the revision of the SWSROP to reflect the
current SW system configuration; 2) the completion of the initial thermal
performance test program for the safety related heat exchangers
c6oled by service
'ater and the establishment of test and/or, cleaning frequencies for them; and (3)
confirmation that the action items from the 1997 SW system SSFI, such as
updating the SW system hydraulic flow model, are being adequately resolved
E8.3
U dated
Unresolved Item 50-244 97-201-02:Valve Testin
Issues
Re ardin
Certain CCW and Sl valves
The specific valve leakage testing concerns were described in Sections E1.2.2.2(d)
and E.1.3.2.2(f) of the Ginna plant design team inspection report 50-244/97-201.
The inspector reviewed these issues with the licensee and cognizant NRR personnel.
URI 97-201-02remains
open pending clarifications of the original inspection
findings among the NRC Office of Nuclear Reactor Regulation (NRR), Region I, and
the licensee concerning the following valves:
~ ~
Regarding the CCW check valves (753ASB) that form the high/low pressure
boundary valves in RCP thermal barrier cooling supply line, the team
considered that these valves should be added to the Ginna Inservice Test
(IST) Program with a leakage testing requirement (i.e., classified as category
A valves).
RGSE sent a letter to the NRC dated November 3, 1997,
clarifying their position to include these valves in the IST program with a
closure verification test and a commitment to add a test connection needed
to perform this test for the 1999 refueling outage.
The licensee reasoned
that leakage testing should not be required since these valves were not
considered to be pressure isolation valves, and since the licensee had
0
periodically tested the relief valves (758A&B)that protect the associated
CCW piping from overpressure.
The inspector verified that 758A&Bhad
been satisfactorily tested during the recent and past refueling outages.
Accordingly, further NRC review of the information regarding the testing of
753A&Bis required.
Regarding the. suction valves (MOVs 896A&B)from the refueling water
storage tank (RWST) to the safety injection (Sl) &. containment spray (CS)
pumps and the valves (MOVs 897 & 898) in the Sl pump recirculation line to
the RWST, the team considered that these valves should have a leakage
.testing requirement in the IST program.
The team considered these valves
comparable to those used as examples in NRC Information Notice 91-56,
"Potential, Radioactive Leakage to Tank Vented to Atmosphere," which
described a'otential leakage path for post-loss of coolant accident (LOCA)
radioactivity to atmosphere through closed emergency core cooling system
(ECCS) pump recirculation valves which were not leakage tested.
The
inspector verified that Revision
1 to the licensee's
IST program added these
valves to be leak tested.
However, in light of possible conflicting information
included in a previous decision regarding leakage testing of similar valves at
another nuclear facility (NRR Memorandum dated May 15, 1995, in response
to Task Interface Agreement 94-22 regarding the H.B. Robinson facility),
further NRC review of information regarding the testing of these MOVs is
required.
No clarifications were needed regarding the check valve (854) in the suction line to
the residual heat removal (RHR) pump from the RWST. The Ginna design team
considered that this valve should be back-flow tested and that a closure verification
test was adequate
(i.e., leakage testing not required);
RG&E agreed to include a
closure verification test in the IST program.
Also, the design team considered that
the containment isolation valves (MOVs 860A,B,C,&D) in the containment spray
system should be leak tested.
RG&E agreed to add an IST leak test requirement to
these MOVs and did leak test these valves satisfactorily'during the recent refueling
outage.
IV. Plant Su
ort
.R8
Miscellaneous RP&C Issues
R8.1
Closed
IFI 50-244 97-06-03:Potential
Si nal Loss of the Meteorolo ical
Monitorin
S stem
In July 1997, inspectors noted a discrepancy between the delta temperature
indication at the site's meteorological tower and in the control room. At that time,
the licensee suggested that the different indications might have been caused by a
signal loss from the tower to the control room. The licensee subsequently
examined its systems and concluded that any actual signal loss would not effect the
control room indications since the system operated with a digital signaI processor.
Reading discrepancies
between the meteorological monitoring tower and the control
C
0
e
'0
room were due to the data processing time (about 2-5 seconds) prior to generating
a readout in the control room.
Based upon the licensee's actions to adequately
resolve this issue, this item is closed (IFI 50-244/97-06-03).
P8
Miscellaneous
EP Issues
P8.1
Closed
IFl 50-244 96-01-03:Call Out Drills
IF 50-244/96-01-03was
opened on May 8, 1996, due to inspector concerns
that the licensee was not able to accomplish all of their response
goals when
performing emergency plan call out drills. Previously conducted drills had
exhibited communications difficulties, and an inability to notify the required
responders within one hour.
On December 8, 1997, the licensee conducted
an off hours unarm'ounced drill with the following objectives:
Demonstrate that the RG&E notification process can notify the required one
hour responders.
Demonstrate that the required one hour responders
can actually respond to
their emergency response facilities.within one hour.
Demonstrate the ability to shift command and control from.the Ginna Control
Room to the Technical Support Center.
All one hour response
positions were staffed within sixty minutes of the
classification of the event and the technical support center assumed
command and
control of the emergency within fiftyminutes of event classification.
The inspectors
concluded that the licensee met the drill objectives and conducted
a successful drill.
'herefore,
this item is closed (IFI 50-244/96-01-03).
S1
Conduct of Security and Safeguards Activities
S1.1
Securit
Pro ram Review
aO
Ins ection Sco
e (81700)
Determine whether the conduct of security and safeguards activities met the
licensee's commitments in the NRC-approved security plan (the Plan) and NRC
regulatory requirements.
Areas inspected were:
access authorization program;
alarm stations; communications; protected area access control of personnel,
packages
and material, and vehicles.
b.
Observations
and Findin s
Access Authorization Pro ram: The inspectors reviewed implementation of the
Access Authorization (AA) program to verify implementation was in accordance
with applicable regulatory requirements and Plan commitments.
The review
included an evaluation of the effectiveness of the AA procedures,
as implemented,
II
0
21
and an examination of AA records for ten individuals.
Records reviewed included
both persons who had been granted and had been denied access.
The AA program,
as implemented, provided assurance that persons granted unescorted
access did not
constitute an unreasonable
risk to the health and safety of the public.
Alarm Stations:
The inspectois observed operations in both the Central Alarm
Station (CAS), and the Secondary Alarm Station (SAS). This observation included
alarm response,
post turnover, and interviews with'the alarm station operators. The
alarm stations were equipped with appropriate alarms, surveillance and
communications capabilities and were continuously manned by knowledgeable
operators.. No single act could remove the plants capability for detecting
a threat
and calling for assistance
because the alarm stations were sufficiently diverse and
independent.
The Central Alarm Statidn (CAS) did not contain any operational
activities that could interfere with the execution of the detection, assessment
and
response functions.,
Communications:
Both alarm stations were capable of maintaining continuous
intercommunications, communications with each security force member (SFM) on
duty, and calling for.assistance
from both on and offsite organizations.
These
comm'unications capabilities have been enhanced
by the recent acquisition and
installation of a new security channel radio repeater.
Protected Area
PA Access Control of Personnel
and Hand-Carried Packa
es:
The
inspector observed operations at the personnel access portal a number of times
during the course of the inspection.
Positive controls were in place to ensure only
authorized individuals were granted access to the PA. All personnel and hand
carried items entering the PA were properly searched
and the last SFM controlling
access to the PA was in a position to perform this function effectively.
PA Access Control of Material: The inspectors observed material processing
in the
warehouse.
The licensee had positive control measures for all materials entering
the PA. Materials entering the PA were identified, searched
and authorized by the
licensee.
Materials entering the PA via the warehouse were searched
by properly
trained and qualified individuals.
PA Access Control of Vehicles: The inspectors observed security operations at the
vehicle entry point including verification of vehicle authorization and performance of
vehicle searches
prior to entry into the PA. The active land vehicle barrier was
operated in accordance with Plan commitments.
The inspectors concluded that
vehicles were being controlled and maintained in accordance with the Plan and
applicable procedures.
Conclusions
The licensee was conducting its security and safeguards activities in a manner that
protected public health and safety and that this portion of the program, as
implemented, met the licensee's commitments and NRC requirements.
II
e
'22
S2
Status of Security Facilities and Equipment
S2.1
Review of Facilities and E ui ment
a 0
Ins ection Sco
e (81700)
Areas inspected were: Testing, maintenance
and compensatory measures;
detection and assessment
aids; personnel and package search equipment and
vehicle barrier systems.
b.
Observations
and Findin s
Testin
Maintenance and Com ensator
Measures:
The inspectors reviewed
testing and.maintenance
records for security-related equipment and found that
documentation was on file to demonstrate that the licensee was testing and
maintaining systems and equipment as committed to in the Plan. A priority status
was being assigned to each work request and repairs were normally being
completed within the same day a work request necessitating
compensatory
~
measures was generated.
The inspectors reviewed'security event logs and
maintenance work requests generated over the last year.
These records indicated
that the need for compensatory measures was extremely minimal. When
necessary,
the licensee implemented compensatory measures that did not reduce
the effectiveness of the security system as it existed prior to the need for the
compensatory measure.
PA Detection and Assessment
Aids: The inspectors observed the licensee's
performance test of the entire Intrusion Detection System (IDS). Allzones of the
IDS were tested, and generated
appropriate alarms.
The test of the IDS was
accomplished
in accordance with the established testing procedure.
The IDS was
functional and effective. The inspectors observed camera coverage, in the CAS and
SAS, of the entire perimeter, while it was being walked down. The camera
coverage and overlap were very good.
The licensee's assessment
aids were
functional and effective.
Personnel and Packa
e Search
E ui ment: The inspectors observed both the
routine use and the daily performance test of the licensee's personnel and package
search equipment.
All search equipment was observed to perform its intended
function.
C.
Conclusions
The licensee's security facilities and equipment were determined to be well
maintained and reliable, and were able to meet the licensee's commitments and
NRC requirements.
'3
S3
Security and Safeguards
Procedures
and Documentation
S3.1
Pro ram and Proceduie Im lementation
a.
Ins ection Sco
e (81700)
Areas inspected were: security program plans, implementing procedures
and
security event logs..
= b.
Observations and Findin s
Securit
Pro ram Plans:
Since the UFSAR does not specifically include security
program requirements, the inspectors compared licensee activities to the NRC-
approved physical security plan, which is the applicable document.
While
performing "the inspection discussed
in this report, the inspectors reviewed the
licensee's
Plan commitments in Section 5.9, titled "Locks, keys, and related
equipment."
The inspectors determined, based on discussions with security
supervision, procedural reviews and observations, that the Lock and Key controls
were effective, properly maintained, and satisfied the requirements of the Plan.
The inspectors verified that selected changes to the Plan associated with the vehicle
barrier system (VBS), as implemented, did not decrease
the effectiveness of the
Plan.
Discussions with the licensee indicated that the plan was currently being
reviewed and a plan revision would be submitted in accordance with the provisions
of 10 CFR 50.54(p) in the near future.
Securit
Pro ram Procedures:
Review of selected implementing procedures
associated with testing and maintenance
and surveillance of personnel search
equipment determined the procedures were consistent with the Plan commitments,
and were properly implemented.
Securit
Event Lo s: The inspectors reviewed the Security Event Log for the
previous six months;-
Based on this rev'iew, and discussion with security
management, it was determined that the licensee appropriately analyzed, tracked,
resolved and documented safeguards
events.
C.
Conclusions
Security and safeguards
procedures
and documentation were being properly
implemented.
Event Logs were being properly maintained, and effectively used to
analyze, track, and resolve safeguards
events.
Lock and key controls were
effectively maintained in accordance with the Plan.
'4
S4
Security and Safeguards Staff Knowledge and Performance
S4.1
Personnel
Performance'.
Ins ection Sco
e (81700)
Areas inspected were security staff requisite knowledge and capabilities to
accomplish their assigned functions.
b.
Observations
and Findin s
Securit
Force Re uisite Knowled e: The inspectors observed
a number of SFMs in
the performance of their routine duties.
These observations included alarm station
operations, personnel and package access control searches,
and PA patrols.
In
addition, interviews were conducted with SFMs and security management.
Finally,
training records were reviewed (see section S5).
Based on all of the above
activities, it was determined that the SFMs were knowledgeable of their
responsibilities.and
duties, and could effectively carry out their assignments..
Res
onse Ca abilities: The inspectors reviewed the licensee's response strategies,
response
drills and critiques and evaluated feedback to the training department for
lessons learned.
c.
Conclusions
The SFMs adequately demonstrated that they have the requisite knowledge
necessary to effectively implement the duties and responsibilities associated with
their position.
The licensee's response
strategies were adequate.
S5
Security and Safeguards Staff Training and Qualification's
S5.1
Trainin
and Qualification TSQ Records Review
a.
Ins ection Sco
e (81700)
Areas inspected were security training and qualifications and training records.
b.
Observations and Findin s
Securit
Trainin
and Qualifications: The inspectors reviewed training records of
ten SFMs. This review indicated that the security force was being trained in
accordance with the approved TSQ plan.
Trainin
Records:
The inspectors'eview of training records determined that the
records were accurate and contained sufficient information to determine the current
qualifications of the individual.
'f
25
c.
Conclusions
Security force personnel were being trained in accordance with the requirements of
the NRC approved TRQ plan. Training records were being properly maintained.
Finally based upon the findings documented
in paragraph S4, the inspector
determined that the training was effective and provided the security force with the
requisite information needed to effectively implement the Plan.
S6
Security'Organization and Administration
S6.1
Mana ement Su
ort of Securit
a.
Ins ection Sco
e (81700)
Areas inspected were: management support, effectiveness
and staffing levels.
b.
Observations
and Findin s
Mana ement Su
ort: The inspectors reviewed various program enhancements
made since the last program inspection to determine the level of management
support.
These enhancements
included the allocation of resources for the following
activities:
- 24 SFMs successfully completed Certified First Responder Trainin'g
- All supervisors attended enhanced
Supervisor Training
- Members of the security staff have attended operational safeguards
response
evaluation (OSRE) exercises at both FitzPatrick and TVA, in preparation for the
Ginna OSRE
- Replacement of all shotguns with new shotguns
- Acquisition and installation of a new metal detector, and a new photo ID badge
video imaging system
- Procurement of additional training aids to enhance tactical response training
Mana ement Effectiveness:
The inspectors reviewed the management
organizational structure and reporting chain.
Security management's
position in the
organizational structure provides a means for making senior management
aware of
programmatic needs.
Senior management's
positive response to requests for
equipment, training and resources
in general have contributed to the effective
administration of the security program.
gati d
immediately available on shift met the requirements specified in the Plan
'6
C.
Conclusions
The level of management support for the security program was adequate,
and was
evidenced by adequate staffing levels and continued resource allocation to improve
training and equipment to enhance effective implementation of the security
program.
t
S7
Quality Assurance in Security and Safeguards Activities
S7.1
Qualit
Assurance Effectiveness
a.
Ins ection Sco
e (81700)
Areas inspected were;
audit/self-assessment
program, problem analyses, corrective
actions and effectiveness of management controls.
b.
Observations and Findin s
Audit Self-Assessment
Pro ram: -The inspectors reviewed licensee security, access
authorization and fitness-for-duty audit report AINT 1997-0010-JMT,for the audit
conducted during the period August 18, 1997, through September 16, 1997.
Five
ACTION Reports were generated
as a result of the audit. The ACTION Reports
were associated with:
Security training lesson plans found to be out of date;
Required procedure. guidance missing from the Employee Assistance
Program;
Health and Human Services (HHS) certified laboratory and testing facility
statistical summary is provided quarterly vs. monthly, as required;
Safeguards Information Access Authorization List Deficiencies; and
Unable to determine whether security communications and duress alarm
~ equipment is Underwriter's Laboratories (UL) and/or Factory Mutual (FM)
listed as required by NRC Inspection Procedure 81088 "Communications."
None of the findings were indicative of major programmatic weaknesses.
The audit
was enhanced
by the use of technical specialists.
Finally, a review of the responses
to the audit findings indicated that the actions taken to address the findings would
enhance program implementation.
The self-assessment
program was well defined and structured.
Self-assessments
were performed in the areas of security operations, access controls, security
systems and training. The licensee performed several self-assessments,
and their
results were well documented.
The data generated was trended, and the results
were well organized.
However, there appeared to be no proceduralized process for
feedback of data generated
by the self-assessment
program.
The benefits of such a
robust self-assessment
program, in terms of program enhancement,
were potentially
negated by this lack of procedural guidance to assure feedback into tlie program.
'7
The licensee agreed to review this portion of the self-assessment
program to
determine if actions were necessary to strengthen this aspect of the program.
Problem Anal ses:
The inspectors reviewed the analyses of data derived from the
self-assessment
program.
The analyses was effective, and problem areas are
trended and identified. Despite the effectiveness of this process,
no proceduralized
feedback system is in place to ensure that resolution to identified problems is
accomplished in all cases.
c.
Corrective Actions: The inspectors reviewed corrective actions implemented by the
liceris'ee in response'to'bo'th
the internal QA audit and in response to the VBS
violation (VIO E97-339).
In both cases, the corrective actions were effective, and
should prevent recurrence of these problems.
F
Effectiveness of Mana ement Controls:
The inspectors observed that the licensee
has a program in place which was effective in identifying, analyzing and resolving
problems.
The corrective actions taken by the licensee,
in response to audit
findings and the VBS violation were adequate
and should prevent recurring
problems.
The. same could be said for the self-assessment
program relative to the
ability of the licensee to identify and analyze problems.
A more proceduralized
methodology for implementing resolution to self identified problems is being
evaluated by the licensee.
Conclusions
The review of the licensee's Audit/Self-Assessment program indicated that the
audits were comprehensive
in scope and depth, that the audit findings were
reported to the appropriate level of management,
and that the program was being
properly administered.
In addition, the corrective actions that were implemented
were effective. The self-assessment
program could be enhanced
by the
.
implementation of a more proceduralized process for ensuring that the results of the
assessments
were effectively used to improve security program implementation.
Miscellaneous Security and Safeguards
Issues
S8.1
Closed
Violation E97-339: Failure to Maintain an Ade uate Vehicle Barrier
a 0
Ins ection Sco
e (TI2515/132)
Areas inspected were the licensee's corrective actions in response to Violation
E97-339.
b.
Observations
and Findin s
Vehicle Barrier S stem VBS: One previously identified violation (VIO E97-339
Failure to Maintain An Adequate Vehicle Barrier) was closed.
The inspectors
reviewed the licensee's corrective actions detailed in their response to the violation,
dated September 15, 1997. Those corrective actions included:
'8
Installation of additional barriers in the areas where openings were identified.
Installation of welded steel plates to prevent removal of cables from their
support poles.
Recalculation of the design bases explosion calculations at distances well
within'the barrier to ensure that proper'protection would be afforded to the
required safe shutdown equipment.
The inspectors walked down the entire VBS, verified the installation of the
additional barriers and welded plates, and reviewed the recalculated design basis
explosive calculations used to determine the safe standoff distances from the VBS
to safety related equipment.
C.
Conclusions
Based upon the inspector's walkdown, as well as a review of the calculations, the
corrective actions were determined to be comprehensive,
effective and fully.
implemented.
This violation is closed (VIO E97-339).
V. Mana ement Meetin s
X1
Exit Meeting Summary
The results of the security inspection were presented
on December 4, 1997, and the
engineering inspection results were presented
on December 17, 1997. After the
inspection period was concluded, the inspectors presented the overall results to members
of licensee management
on January 9, 1998. The licensee acknowledged the findings
presented.
The inspectors asked the licensee whether any materials examined during the inspection
should be considered proprietary.
No proprietary information was identified.
L2
Review of UFSAR Commitments
While performing the inspections discussed
in this report, the inspector reviewed the
applicable portions of the UFSAR that related to the areas inspected.
The inspector
verified that the UFSAR wording was consistent with the observed plant practices,
procedure and/or parameters.
~I
ATTACHMENTI
PARTIALLIST OF PERSONS CONTACTED
Licensee
R. Albrecht
B. Flynn
C. Forkell
G. Graus
A. Harhay
J. Hotchkiss
G. Joss,
R. Marchionda
G. Palmer
P. Polfleit.
T. Porter
R. Ploof
J. Smith
R. Teed
J. Trayner
J. Widay
T. White
G. Wrobel
Training Supervisor
Primary'Systems
Engineering Manager
Electrical Systems Engineering Manager
IRC/Electrical Maintenance Manager
Chemistry 5 Radiological Protection Manager
Mechanical Maintenance Manager
,Results and Test Supervisor
Production Superintendent
Security Operations Coordinator
Mana'ger
Nuclear Security System Specialist
Secondary Systems Engineering Manager
Maintenance Superintendent
Supervisor, Nuclear Security-
Senior QA Analyst
Plant Manager
Operations Manager
Nuclear Safety 5 Licensing Manager
INSPECTION PROCEDURES USED
IP. 37551:
IP 61726:
IP 62707:
IP 64704:
IP 71707:
IP 71750'P
92903:
IP 92904:
IP 81700:
TI251 5/1 32:
Onsite Engineering
Surveillance Observation
Maintenance Observation
Plant Operations
Plant Support
Follow-up - Engineering
Follow-up - Plant Support
Physical Security Program for Power Reactors
Malevolent Use of Vehicles at Nuclear Power Plants
Attachment
I
ITEMS OPENED, CLOSED, AND DISCUSSED
~Oened
VIO 97-12-01
Failure to Follow Administrative Procedure Requirements
e
IFI 97-12-02
Determine Appropriate Operability Parameters for the EDGs
Closed
VIO 96-06-02;,
Inadequate Safety Evaluation Regarding Stroke Time Change for
MOV-461 6 .
I
VIO E97-'339
LER 97-002
Failure to Maintain an Adequate Vehicle Barrier
Loss of 34.5 KV Offsite Power Circuit 751, Due to External Cause,
Results in Automatic Start of "8" Emergency Diesel Generator
LER 97-004
LER 97-005
LER 97-006
Radiation Monitor Alarm, Due to Higher than Normal Radioactive Gas
Concentration, Results in Containment Ventilation Isolation
e
Undetected Unblocking of Safety Injection Actuation Signal While at
Low Pressure Condition, Due to Faulty Bistable, Resulted in
Inadvertent Safety Injection Actuation Signal
Verification of Boron Concentration Not Performed Due to
Misinterpretation of Event Sequence,
Resulted in Condition Prohibited
by Technical Specifications
LER 97-007
Reactor Trip Instrumentation Would Have Been in a Condition
Prohibited by Technical Specifications
IFI 97-06-03
IFI 96-01-03
Potential Signal Loss of the Meteorological Monitoring System
Call Out Drills
Discussed
URI 96-06-04
URI 97-201-02
Service Water System Reliability Optimization Issues
CCW and Sl System Valve Testing Issues
Attachment
I
3
LIST OF ACRONYMS USED
CATS
CFR
CRFC
d/p
EDGE
GL
IFI
IR
KV
KW
LCO
LER
NRC
OSRE
psi
psIg
RG&E
RPS.C
AuxiliaryFeedwater
ACTION Report
American Society of Mechanical Engineers
Commitment Action Tracking System
Central. Alarm System..
Component Cooling Water
Code of Federal Regulations
Containment Recirculation Fan Cooler
Design Basis Documentation
differential pressure
Engineered Safety Feature
Generic Letter
Intrusion Detection Systems
Inspector Follow-up Item
Inspection Report
Inservice Inspection
Inservice Test
Improved Technical Specification
Kilovolts
Kilowatts
Limiting Condition for Operation
Licensee Event Report
Loss of Coolant Accident
'otor-Operated Valve
Nuclear Regulatory Commission
Nuclear Reactor Regulation
Operator Safeguards
Response
Exercises
Protected Area
Procedure Change Notice
'lant
Change Request
Public Document Room
Preventive Maintenance
Plant Operations Review Committee
Probabilistic Safety Analysis
pounds per square inch
pounds per square inch gauge
Periodic Test
Quality Assurance
Quality Control
Radiologically Controlled Area
Reactor Coolant Pump
Rochester Gas and Electric Corporation
Radiation Protection
Radiological Protection and Chemistry
C
~ g
Attachment
j
~
SAFW
SEV
SFM
Sl
Tave
T&Q
The Plan
UL
I
4
Resistance Temperature Detector
Refueling Water Storage Tank
Standby Auxiliary Feedwater
Secondary Alarm System
Safety Evaluation
Security Force Members
Safety Injection
Safety System Functional Inspection
Service Water System Reliability Optimization Program
Primary Coolant System Average Temperature
Training and Qualific'ation
NRC-Approved Physical Security Plan
Updated Final Safety Analysis Report
'nderwriter's
Laboratory
Unresolved Item
Vehicle Barrier System
Violation
jl