ML17229A766
| ML17229A766 | |
| Person / Time | |
|---|---|
| Site: | Saint Lucie |
| Issue date: | 06/08/1998 |
| From: | Schin R NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML17229A764 | List: |
| References | |
| 50-335-98-06, 50-335-98-6, 50-389-98-06, 50-389-98-6, NUDOCS 9806160218 | |
| Download: ML17229A766 (73) | |
See also: IR 05000335/1998006
Text
U.S.
NUCLEAR REGULATORY COMMISSION
REGION II
Docket Nos: 50-335,
50-389
License
Nos:
Report Nos: 50-335/98-06.
50-389/98-06
Licensee:
Florida Power
5 Light Co.
Facility:
St. Lucie Nuclear Plant, Units
1
8
2
Location:
6351 South
Ocean Drive
Jensen
Beach,
FL
34957
.
Dates:
March 29 - May 9,
1998
Inspectors:
M. Miller, Senior Resident
Inspector
J.
Munday, Acting Senior
Resident
Inspector
D. Lanyi. Resident
Inspector
G. Warnick, Resident
Inspector
J. York. Regional
Inspector
(Section E2.2)
C. Patterson,
Senior Resident
Inspector,
Brunswick
(Section 07)
P. Kellogg, Regional
Inspector
(Sections
El. 1 and
E8.1)
M. Holbrook,
INEEL Contractor,
(Sections
El. 1 and
E8.1)
G. Wiseman,
Regional
Inspector
(Section F2.1)
E.
Brown. Resident
Inspector,
Brunswick (Section 07)
Approved by:
R.
P. Schin, Acting Chief,
~ Reactor Projects
Branch
3
Division of Reactor Projects
980bi602i8 9'8Q608
ADQCK 05000335
8
e
EXECUTIVE SUMMARY
St. Lucie Nuclear Plant, Units
1
& 2
NRC Inspection Report 50-335/98-06.
50-389/98-06
This integrated
inspection included aspects
of licensee operations,
engineer-
ing, maintenance,
and plant support.
The report covers
a 6-week period of
resident inspection.
In addition, it includes the results
from inspection of
the licensee's
corrective action and self-assessment
program
as well as
identifying completion of the implementation of Generic Letter 89-10, "Safety-
Related Motor-Operator Valve Testing
and Surveillance."
~0erations
~
Three equipment clearance
errors occurred during this report period arid
represented
multiple errors that have occurred since January
1997.
Previous corrective action had not been adequate to arrest the problem.
Additional corrective
actions were planned in response to these three
errors.
This issue
was identified as
a repetitive violation.
(Section
01.2)
~
An inspector
walkdown of the Unit 1 waste
gas system identified only
minor discrepancies
that were addressed
by the licensee.
A Non-Cited
Violation was identified because of a licensee-identified
noncompliance
with the Technical Specification 4. 11.2.5. 1 requi rement for continuous
monitoring of oxygen in the in-service waste
gas
decay tank.
This
Technical Specification for both units had previously been revised
and
administrative errors
made
as part of 'the revision resulted in the
specification being inadequate.
At the close of the report period the
licensee
was in the process of submitting another
Technical
Specification
amendment
request.
(Section 02. 1)
~
The inspector concluded that reactor
operator trainees
were not spending
an appropriate
amount of time performing control
room duties
under 'the
direction of a licensed operator.
Discussion with the licensee training
staff and management
indicated that the reactor
operator on-shift
training program was not being implemented
as designed.
The licensee
took action to ensure the required
amount of On the Job Training was
provided.
(Section 05. 1)
~
.
The Corrective Action, Operating Experience
Review, Quality Assurance
and Self-Assessment'rograms
were reviewed in accordance
with Inspection
Procedure
40500.
Favorable trends were noted in site activities.
Problem identification was effective and on-site/off-site safety review
,
committees
provided effective safety oversight.
(Section 07.1)
~
The corrective action program lacked
a focus
on correction of problems.
Several
examples of recent Condition Reports indicated that timely
corrective action for
a 1997 Quality Assurance audit was not effective.
The inspectors identified
a violation with three examples
in the area of
corrective actions.
The examples
were:
1) untimely implementation of
corrective action,
2) inadequate
corrective action,
and 3) root cause
evaluations
not performed
as required
by controlling procedures.
(Section 07.6)
2
~
The inspector considered
the operator performance of a surveillance of
control element assemblies
to be excellent.
The control
room was quiet
with little other activities
or traffic.
Oversight of operators
in
training during this evolution was also excellent.
(Section 08. 1)
Maintenance
~
The inspector
concluded that the licensee's
method of Work Order
planning was adequate,
but placed
a heavy reliance
on the skill of the
maintenance
worker
and supervisory oversight.
The inspector
did not
identify examples
where this reliance resulted in inadequate
work.
In
addition, the inspector
concluded that procedure
GNP-21 provided an
excellent tool for developing work instructions
and controlling
troubleshooting of equipment
problems.
(Section Ml.1)
~
The experience
and thoroughness
of the maintenance
and operations
personnel
helped identify a procedural
error involving the testing of
safety components
on Unit 2 during performance of an Engineered
Safeguards
Actuation System test.
The inspector
concluded that the
correct actions were taken when the error
was identified and were
properly< per formed.
(Section Ml.2)
En ineerin
'he
NRC staff review of the Generic Letter 89-10 program at St. Lucie
was closed
based
on the completed
and scheduled
work, including the
actions identified in the Plant Manager's Action Items.
The completion
of the commitments in the Plant Manager's Action Items
and the closure
of the remaining items will be tracked
as
an Inspector
Follow-up Item.
(Section El.l, E8.1)
Upon identification, the System
and Component
Engineer actively worked
toward correcting deficiencies with the Unit 1 Sodium Hydroxide tank
level indication.
The inspector noted good communications
between the
System
and Component
Engineer
and Chemistry .in determining the problem
and corrective actions.
A weakness
was identified when Operations
and
18C failed to inform Chemistry or the System
and Component
Engineer
about the results of work performed
on the level instrument.
(Section
E2.1)
~
The licensee
has adequately controlled, in a timely manner,
the safety-
related information in the Total Equipment Database.
The licensee's
new
updating process
was adequate
and facilitated
a more'imely resolution
of non-safety-.related
setpoints
and other design information issues
as
they are found in the Total Equipment Database.
The licensee
was
allocating substantial
engineering effort to resolve the problems with
the Total Equipment
Database
and to improve the support for the
18C
group maintenance
setpoint
and calibration program.
(Section E2.2)
i
~Pi
tS
t
~
An NRC inspection of the fire protection water system identified that
the maintenance
and material condition of the system
components
and fire
pumps
was good.
There was not
a high backlog of open work orders
associated
with the fire protection water system
components
or the fire
pumps'.
The number of open Condition Report deficiencies identified as
part of the station problem evaluation process
associated
with the fire
rotection water system, components
or the fire pumps
was small.
The
icensee's
corrective action dispostioned for resolution of fire
protection system problems
was being properly scheduled.
(Section
F2. 1)
Re ort Details
Summar
of Plant Status
Both units operated
at essential)y full power for the entire report period.
01
01.1
Conduct of Operations
General
Comments
71707
I. 0 erations
01.2
Using Inspection
Procedure
71707. the inspectors
conducted
frequent
reviews of ongoing plant operations.
In general,
the conduct of opera-
tions was professional
and safety-conscious;
specific events
and
noteworthy observations
are detailed in the sections
below.
E ui ment Clearance
Order Problems
Ins ection Sco
e
71707
92901
The inspector evaluated three
Equipment Clearance
Order
(ECO) problems
identified by the licensee
from February.19 through March 31.
The
inspector
reviewed the root cause
analyses,
the corrective actions
taken,
and the generic implications.
Observations
and Findin s
From February
19 through March 31, the licensee identified three
significant
ECO errors.
The licensee
generated
condition reports
and
performed root cause
analyses
for each occurrence.
On February
19, the licensee
was preparing Unit 1 for operations
following a Reactor Coolant
Pump
(RCP) seal
replacement.
While removing
the
ECO
(ECO 1-98-01-202S) for the
1B2 RCP, the Non-licensed Operator
. (NLO) informed his supervisor that he had accessed
the
1B1
RCP to
release
the clearance.
Then, the supervisor
and
NLO discovered that the
clearance
had been inadequate
in that seal injection to the wrong pump
had been isolated.
The licensee's
investigation identified the following sequence
of
events.
On February 5. the Clearance
Center originated the
ECO.
This
version of the clearance correctly isolated the
1B2 seal injection line.
When the unit was brought off line on February
16. the clearance
was
printed and prepared for hanging.
The next day, the Operations
Supervisor
reviewed the clearance
and suggested
that the valve upstream
of the one identified in the clearance
should
be used to isolate seal
injection.
The Clearance
Super visor agreed to change the
ECO.
The
clearance writer inadvertently entered
V20302 as the seal injection
isolation for the 182
RCP.
The correct valve number was V30303.
The
computer
system accurately entered the remainder of the descriptor
as
the isolation for the
1B1
RCP seal injection.
The supervisor failed to
2
note this on the clearance
form and highlighted the correct valve on the
llx17 print.
The supervisor
reviewing and authorizing the clearance failed to note
the discrepancy
on the
ECO form.
His review of the highlighted valves
on the Print showed that the proper valves were going to be manipulated.
The fie1d operator selected to hang the clearance,
correctly hung the
tags
on the valves.
The operator
was concurrently involved in hanging
hoses for seal
bleed off'on all
RCPs.
He, therefore.
did not recognize
that tagging the seal injection valves for the
1B1
RCP was
inappropriate.
The on-shift Assistant
Nuclear Plant Supervisor
(ANPS)
waived the independent verification due to ALARA concern,
although the
area
was not
At no time in the Maintenance
walkdowns of the clearance
was this
discrepancy
thought to be
a problem.
Three different Maintenance
foremen held the clearance
and numerous
journeymen worked on the pump.
At least
one journeyman noticed the
1B1
RCP valve on the clearance,
but
did not pursue the reason.
The licensee's
root cause analysis for the
RCP clearance error suggested
that scheduling pressures.
inadequate
clearance
center staffing.
and
excessive
congestion in the clearance
center contributed to the problem.
However, the licensee identified personnel
error, particularly by the
reviewer,
hanger,
and authorizer,
as the prime cause of the error.
The
licensee's
corrective actions were diverse,
in that they provided
correction to most identified weaknesses.
However. they did not provide
any mechanism to track the correction of inadequate staffing.
On March 30, the licensee identified that
a grounding device was
installed in the
2C intake cooling water
( ICW) pump breaker cubicle for
planned maintenance.
However, the grounding device was never documented
in the supporting
ECO, 2-98-03-005,
as required
by procedure
ADM 09.04.
Revision 3, "In-Plant Equipment Clearance
Orders."
The licensee
determined that the Electrical
Maintenance
Department's
guidance
on
installation of ground test devices
was not fully compatible with the
ECO procedure in that the guideline did not specify that
a
jumper/grounding device should
be identified on
a clearance.
The
licensee's
corrective action was to revise the guidelines to ensure that
the Work Control
Super visor was aware of the grounding device.
On March 31, the licensee identified an inadvertent
gas release
from the
waste gas
system to the Reactor Auxiliary Building (RAB).
During
maintenance of the
2B Waste
Gas Compressor.
the Maintenance
Crew removed
the filter cover of the compressor
and noted that pressurized
gas
was
escaping into the Reactor Auxiliary Building.
At first, they believed
that the gas
was residual
gas being released.'hen
the
NLO arrived,
he
shut the inlet and outlet valves to the compressor to secure the
release.
The licensee
determined that the Clearance
request
did not
identify that the maintenance
required breaking into the system.
Therefore,
only the compressor's
breaker
was tagged.
The inspectors
reviewed the licensee's
recent performance in the area of
Clearance
Control
and noted that similar personnel
problems
kept
recurring.
The table below summarizes
the findings.
VIO Number
97-01-01
97-03-01
97-04-01
97-06-01
NCY
97-14-03
Event Description
Two lifted leads
were incorrectly
identified and then mistagged.
Personnel
error
Charging
pump discharge
seal
tank
leak caused
by vent valve tagged
open with a tag that had been
removed from the clearance
form.
Personnel
error
1. Circulating
Water
Pump worked
with the breaker
NOT tagged:
2. Diesel lube oil pump untagged
with an open
Work Order in place.
3. Clearance
being hung for
Thermolag work.
Wrong Hotor
Control Center tagged.
4.'learance
for reactor drain
down not adequate.
Spilled 500
gallons in Reactor Auxiliary
Building.
Personnel
error
1.
Low Pressure
Safety Injection
suction check valve work started
before clearance
hung.
Cognitive error
1.
Volume Control Tank hydrogen
line drain left open.
Personnel
error
2. Tagless
clearance
violated
when Reactor Coolant System level
raised too high.
Process error
Personnel
error
Corrective Actions
1. Clearance
procedure
changed to
add requirements to seek help from
other groups to read Electrical
Drawings.
2. Discussed
in requalification
training need to pay attention to
the details.
3. Haintenance
Training on
attention to detai l.
1. Procedural
enhancements.
2. Operator training.
1. Clearance
Center scheduling
enhancements.
2. Plan of the Day upgrades.
3. Procedure
enhancements.
4. Operator,
Planner.
and
Haintenance
personnel training.
5.
Made field size drawings
available.
l. Operations briefing.
2. Clearance
stop work order
issued.
3. All clearances
in field
verified.
4. Hanagement
Independent
Verification of all new clearances
hung.
1. Procedure
change controlled
clearance
changes
better.
2. Licensee updating clearance
computer software.
3. Procedure
change put better
control on tagless
clearances.
VIO Number
98-06-01
Event Oescription
1. Tagged wrong Reactor Coolant
Pump seal injection.
Personnel
error
2. Grounding device for 2C
ICW
pump breaker not shown on
clearance.
Process error
Personnel
error
3. Inadequate
waste
gas
system
tagout resulted in gas release.
Per sonnel
er ror
Corrective Actions
1. Planned to remodel the Work
Control Center to reroute traffic
patterns.
2. Assigned extra licensed
personnel
to perform clearance
tasks.
3. Stand
down meetings.
The licensee identified an unsatisfactory trend in
ECO implementation in
their
1996 Fourth Quarter Condition Report Trend.
On July 25.
1997, the
licensee
completed their root cause analysis
and issued
a report listing
all identified causal
factors
and generic weaknesses.
The licensee
revised the
ECO procedure.
However, only eight of the 30 recommended
corrective actions were carried out.
The licensee
determined that the
remaining actions would =not be effective from a cost-benefit analysis.
None of the
recommended
actions to address
generic implications nor
any
measures
to evaluate the effectiveness
of the corrective actions were
done.
The inspector
noted that the latest
ECO problems were similar in
nature to those cited in VIO 97-04-01.
The corrective actions that were
suggested
attempted to ensure that all personnel
involved in the
clearance
process
were fully aware of all requirements,
and that there
was more control
on the up front clearance
planning process.
Technical Specification 6.8. 1 requires the licensee to establish,
implement.
and maintain the applicable procedures
recommended
in
Appendix A of Regulatory Guide 1.33.
Equipment Control (e.g.. tagging
and locking) is covered
by this Appendix.
The licensee's
implementing
procedure
was procedure
ADM-09.04, Revision 3, "In-Plant Equipment
Clearance
Orders."
Section 3.8.3 required Electrical Department
Personnel
to "Verify that any grounding device is documented
on the
Equipment Clearance
Order Form as
a step with'no tag."
Section 6.8.4.A
required the Nuclear Plant Supervisor
(NPS), Assistant
(ANPS), the
Work Control Center-ANPS,
or the Nuclear Watch Engineer
(NWE) "shall
verify
.
.
. the adequacy of the information contained in the request
section of the
ECO Control Form."
Section 6.9.2.C required the Reactor
Control Operator
(RCO) to "Verify [the] boundary using controlled
documents.
.
. ."
Section 6. 11. 1.A required the
NPS,
ANPS,
NWE,
WCC-
ANPS
~ or a Senior Reactor Operator
licensed
RCO to "Verify the specified
ECO boundary satisfies the requirements
specified in the
ECO request."
~
Section
6. 12.20.A required the
ECO Controller to sign the
ECO Control
Form when they find the
ECO acceptable.
Section
6. 12.20.B stated
"Signing the Acceptance
Block on the Equipment Clearance
Order Form
(Figure 1) indicates
concurrence that the
ECO boundary is adequate
for
the work to be performed."
Finally, Section
6. 12.23.A required the
workers to perform
a
verification of the
ECO boundary utilizing
available
reference materials."
For the three examples
above,
the
licensee failed to perform all of the above steps
adequately.
This is
02
02.1
b.
considered
a repeat of VIO 50-389/97-04-01
and is identified as
VIO 50-
335.389/98-06-01,
"Repeat Failure to Implement
an Equipment Clearance
Order Prior to Beginning Work."
The licensee's
response to the repetetiveness
of the most recent
clearance errors,
as addressed
in VIO 335,389/98-06-01,
was to have the
Operations
Hanager observe the Clearance
Center for
a week.
From this
observation,
the licensee
chose to carry out several significant planned
changes.
First. the licensee
planned to remodel the Work Control Center
to reroute traffic patterns.
The licensee
believed that this would
allow the, Work Control Personnel
to concentrate
on their tasks better.
Also, the licensee
determined that they would assign extra licensed
personnel
to perform clearance
tasks.
This would reduce the burden
on
the remainder of the staff,
and,
according to the licensee.
allow better
quality clearances.
The licensee
continued their stand
down meetings
with all operations
personnel,
reiterating the importance of zero
defects in clearances.
Conclusions
Three equipment clearance
errors occurred during this report period and
represented
multiple errors that have occurred since January
1997.
Previous corrective action had'not
been adequate to arrest the problem.
Additional corrective actions
are planned in response to these three
errors.
This issue is identified as
a repetitive violation.
Operational
Status of Facilities and Equipment
Unit 1 Waste
Gas
S stem Walkdown
Ins ection Sco
e
71707
The inspector walked down accessible
portions of the Unit 1 waste
gas
system including the Oxygen Analyzers
and
reviewed the applicable procedures.
Observations
and Findin s
The inspector
reviewed Procedure
OP 1-0530020.
Revision 31,
"Waste
Gas
System Operation,"
Drawing 8770-G-078,
Sheet
163A,
and walked down the
system in the field.
The inspector
found eight valves identified as
normally open
on the drawings that were actually normally closed.
Also,
the inspector identified six valves that may not have been aligned by
any procedure
and
a valve in a
common drain line that did not appear
on
any drawing.
The valves that were not included in a procedure could not
have caused
an accidental
release of waste gas.
Two other minor human
factors deficiencies
were noted.
These discrepancies
were forwarded to
the System Engineer for resolution.
The inspector verified that the procedure to place
a gas
decay tank
(GDT) in or out of service would work as written.
Later, the inspector
observed
a Non-licensed Operator
(NLO) performing this task.
The
NLO '
7
was knowledgeable of the procedure
and secured
one tank and placed
another in service.
The inspector
noted that the
NLO contacted
Health
Physics prior -to starting the evolution.
t
The licensee
has
had recent problems with leakage in the waste
gas
system.
In fact the licensee
secured
the oxygen (0,) analyzers
several
times during the report period in an attempt to isolate leakage.
Several
minor leaks were identified by the licensee
on the 0, analyzers,
but the major source of th'e leaks
was due to valves associated
with the
waste
gas compressors.
However, during this time, the licensee
identified that
a Technical Specification
(TS) surveillance required
continuous
oxygen monitoring for the 'in service
GDT.
TS 4. 11.2.5. 1
required that "The concentration of oxygen in the waste
gas decay tank
shall
be determined to be within the above limits by continuously
monitoring the waste
gases
in the on service waste
gas
decay tank."
Unit 2 0, analyzer,
2-6602,
has
been out of service since
1989 due to
'arious
reasons
(parts.
procedure
upgrades.
etc.).
On April 30,
2-6601
failed.
No gas analyzer
was monitoring oxygen levels in the in service
GDT.
The licensee realized that this was not in accordance
with the TS
surveillance.
Licensing issued
a Condition Report
(CR) to document the
problem and started preparing
a Licensee
Event Report
(LER) to report
the condition prohibited by TS.
Meanwhile, the licensee
gathered
information as to the cause of the event.
The licensee
determined
several salient points.
First, in December
1995,
TS were amended to
move all waste
gas
system references
from TS into the
FSAR.
This was
completed with the following revision of the
FSAR.
At that time TS
4. 11.2.5. 1 had
a note stating if continuous monitoring of GDTs was
unavailable,
grab samples in accordance
with a table was allowed.
This
table was
no longer found in TS, but had been
moved to the
FSAR.
Approximately one year later.
an administrative
change to TS was
made
that eliminated the note.
Therefore.
whenever both 0
analyzers
in a
unit were unavailable.
the licensee
was unable to meek their TS
survei 1 1 ance requirements.
Second,
Unit 1 had been in this condition at least
once earlier, in
April.
The licensee
had been isolating the gas analyzers
in 'an attempt
at finding the gas leaks.
The licensee
was continuing to research
historical records for other examples.
Third,
up until about a'year
and
a half ago. the licensee did not routinely use their
GDTs.
Standard
~
~
rocedure
was to vent directly to the stack.
Although not prohibited by
S. this practice
was determined to be undesirable
because it could
result in higher radioactive release
rates.
The licensee
determined that
a TS amendment
was required to return the
TS to its original intent and started processing
the request.
Meanwhile, they have acknowledged that if both 0, analyzers
become out
of service
on
a unit, they would have to vent directly to the stack to
avoid violating the current
TS requirement.
Additionally, the
licensee'as
working on restoring both Unit 2 0, analyzers.
This non-repetitive,
licensee identified and corrected violation is being treated
.as
a Non-
Cited Violation. consistent with Section VII.B of the
NRC Enforcement
Policy,
and is identified as
NCV 50-335,389/98-06-02,
"Failure to
Fulfill a Technical Specification Surveillance
Requirement to
Continuously Monitor Oxygen Concentration in the Gas
Decay Tank."
c.
Conclusions
An inspector
walkdown of the Unit 1 waste
gas
system identified only
minor discrepancies
which were addressed
by the licensee.
An NCV was
identified because of a licensee-identified
non-compliance with the TS
4. 11.2.5. 1 requirement.
This TS for both units had previously been
revised
and administrative errors
made
as part of the revision resulted
in the specification being inadequate.
At the close of the report
period the licensee
was in the process of submitting another
TS
amendment
request.
02:2
Shield Bui ldin
Ventilation
S stem Walkdown
Unit 1
Ins ection Sco
e
71707
The inspector performed
a walkdown of accessible
portions of the Shield
Building Ventilation System.
Additionally, the inspector
reviewed
recent surveillance
records
documenting the testing of the filter train
and the associated
results.
Observations
and Findin s
The inspector
reviewed Section 6.3.2 of the Updated Final Safety
Analysis Report
(UFSAR) and compared it with Technical Specification
(TS), Section 3/4.6.6, to verify adequacy.
Drawing 8770-G-879,
Sheet
2,
was used to perform the system walkdown.
Also, Procedure
1-NOP-25.01,
Revision 0, "Shield Building Ventilation Operation"
was reviewed by the
inspector to verify the system line up.
The inspector noted
a minor discrepancy
regarding the procedural
requirement for the position of FCV-25-13.
Procedure
1-NOP-25.01,
Rev.
0, required that the valve be in the position of NORM/OPEN.
However,
the switch, position on the control panel
was
a "spring return to the mid
position".
This mid position on the switch had no inscription which
could potentially lead to operator confusion.
The inspector
informed
the system engineer of the discrepancy for evaluation.
The inspector
reviewed surveillance
records for the testing of the
shield building ventilation filtering system.
The frequency of test
performance
and the results obtained
met the
TS requirements.
Conclusions
Equipment operability. material conditions,
housekeeping,
and
surveillance
records
were acceptable.
05
05.1
Re uired Postin
s
71707
The inspector verified that all information required
by 10 CFR 19.11
was
posted.
The licensee controlled the required postings with procedure
AP-0010721
NRC Required
Non-Routine Notifications and Reports,"
Revision 38.
The procedure
required
NRC Form 3 and four appendices
from
the procedure
be posted in five areas.
The inspector verified that all
areas
were posted
and that the posted information met all requirements
of Part 19.
The licensee
met all posting requirements of 10 CFR 19.11.
Oper ator Training and Qualification
On-shi ft Tr ainin
of Reactor
0 erator Trainees
Ins ection Sco
e
71707
During this report period the inspector
reviewed the licensee's
on-shift
training program for the reactor operator trainees.
The inspector
reviewed Administrative Procedure
0005721,
Revision 17. "Reactor Control
Operator Training and Qualification", several
On The Job Training (OJT)
guides,
discussed
the program. with several
trainees
and witnessed
training during Control
Element Assembly
(CEA) testing.
Observations
and Findin s
During this report period the inspector often noted that the reactor
operator trainees
on shift were not working in the control
room, but
rather
were studying elsewhere.
The inspector
discussed this with many
of the tr ainees
and concluded that during the time spent on-shift many
. requirements
had to be completed.
OJT guides.
consisting of knowledge
requirements
(questions
and answers),
activities requirements
(locating
equipment
or reading drawings),
and practical
requi rements
(performing
or simulating actual
equipment manipulations)
were to be completed while
on shift.
Nany of the trainees
were spending
a great deal of time
studying procedures
and reviewing plant material related to these guides
outside of the control
room rather than completing the guides
under the
di rection of licensed operators while in the control
room.
The
inspector
noted
on several
occasions. critical activities were completed
without affording the trainees
the opportunity to get involved.
One
example occurred
on Unit 1 when the plant computer
became
Licensed operators
had to perform troubleshooting
on the system,
but did
so without the added benefit of trainee
involvement.
The inspector
reviewed the operator logs to determine
when the trainees actually stood
watch in the control
room and noted that often their names
would not
appear in the logs.
The inspector
reviewed Procedure
AP 0005721,
Revision 17, "Reactor
Control Operator Training And Qualification," and noted that step 8.1.4
stated
"a minimum of 13 weeks
(65 days) shall
be completed
as
an extra
person
on shift in training for the
RCO position.
This training should
include all phases of day-to-day operations activities and shall
be
completed
under
the direct supervision of licensed personnel."
The
07
07.1
07.2
9
inspector verified this to be consistent with existing
NRC regulatory
guidance.
The inspector
expressed
the concern with both Operations
management
and Training personnel
that these
requirements
might not be
getting satisfied.
The licensee stated that the on-shift portion of the
training was intended to be conducted with a trainee standing watch
under the guidance of a licensed operator in each unit's control
room
each shift.
The other trainees
were to witness,
perform or simulate
various activities in the control
room as described
in the G3T guides or
as plant conditions allowed.
Although review of procedures,
drawings
and other technical
manuals
was expected to occur outside the control
room on occasion,
the trainees
were meant to spend the majority of their
time interacting with licensed operators
and their mentor.
The licensee
reiterated
these expectations
with the trainees
and their mentors.
Toward the end of the report period the inspector
noted
much improvement
in the on-shift training.
On April 29, the inspector witnessed trainees
performing
CEA testing.
This is discussed
in section
08. 1 of this
report.
Conclusions
The inspector concluded that reactor operator
trainees
were not spending,
an appropriate
amount of time performing control
room duties
under the
'irection of a licensed operator.
Discussion with the licensee training
staf'f and management
indicated that the reactor operator on-shift
training program was not being implemented
as designed.
The licensee
took action to ensure the required
amount of OJT was provided.
Quality Assurance in Operations
General
Comments
40500
Using inspection procedure
40500 'Effectiveness
of Licensee Controls"
in Identifying, Resolving,
and Preventing
Problems,
an inspection
was
conducted of the licensee's
corrective action program,
operating
experience
review, self-assessments
and quality assurance
(QA). and on-
site/off-site safety review committees.
Generally,
favorable trends
were noted in site activities.
Problem identification was effective.
On-site/off-site safety review committees
provided effective safety
oversight.
However, the corrective action program lacked focus
on
correction of problems.
Several
examples of recent Condition Reports
(CRs) in 1998 indicated that timely corrective action for a 1997
licensee
QA audit concerning corrective action was not effective.
This
was identified as
a corrective action violation.
P
Trendin
Pro
ram
Ins ection Sco
e
40500
The inspector
reviewed the effectiveness
of licensee trend
identification and response.
10
Observations
and Findin s
A list of CRs was reviewed by the inspector.
The
CRs identified
deficiencies in several
areas
including:
procedural
adequacy,
control
and adherence
clearances
fire protection
design drawings
emergency
response
organizational staffing
The use of initiation codes for the analysis of trends
allowed the
licensee to tabulate trends in some areas of human performance
and
equipment related events.
Review of the quarterly trend reports for
1997 indicated adequate identification of trends for that quarter,
and
the trends were consistent with the inspector's
findings.
The inspector
noted that the resolution of significant negative trends identified in
previous reports were not consistently
reviewed in subsequent
reports.
Therefore,
the 'effectiveness
of actions taken
was not evident.
Likewise, the inspector
noted that action items initiated at the request
of management
were not consistently
reviewed
and updated.
The second
quarter trend report indicated that the results
were not presented to
management.
The licensee stated that the issuance of the trend reports
for several
quarters in 1997 had not been timely and that management
had
not always
been briefed on the results.
One trend report was issued
approximately six months after the end of the quarter.
The licensee
related that
a self-assessment
was underway to assist in improving the
effectiveness
of the program.
Discussions with the licensee
revealed that the identification of
repetitive issues
would reside in the trending program as
a result of a
pending
change in the corrective action program.
However, the licensee
indicated that the administration of the trending program was not
covered
by any procedural
guidance.
The inspectors
concluded that
without procedural
guidance the trending program
may lack consistency
and 'become less effective.
Conclusion
The quarterly trend reports adequately identified site trends.
The
effectiveness
of these reports
was diminished by the lateness
of report
issuance
and communication to site supervision.
There was
a lack of
procedural
guidance for trending nonconforming issues.
Problem Identification and Characterization
Ins ection Sco
e
40500
The inspector
reviewed
CRs for adequacy of problem identification and
"
proper characterization
in accordance
with the guidance provided in
Administrative Procedure
AP-0006130.
Revision 12, "Condition Reports."
11
b.
Observations
and Findin s
The inspector
reviewed
CRs and Plant Manager Action Items
(PMAIs)
~
initiated from March 1997 to present.
The inspector determined that the
CR initiation threshold
was sufficient to assure
adequate identification
of nonconforming conditions.
Depending
on the source.
the condition may
be entered into the
CR program or PMAI database.
Certain items.
such
as
the need for procedural
revisions
and
UFSAR discrepancies
changes,
could
bypass the
CR process
and be entered directly as
a PMAI.
The licensee's
program established
characterization
and set the duration
for problem analysis of the issues
based
on severity level
and analysis
technique.
The severity level
was primarily based
on reportability and
operability.
For items requiring reportability or operability
assessments,
a 3-day level was assigned.
Reportability assessments
without operability concerns
were, assigned
a 10-day level.
Issues that
did not require either
an operability or reportabi lity assessment
were
assigned
a 30-day level.
'A fourth level designated
as other, included
any condition that did not meet the 3-day or 10-day criteria but
requi red resolution in less than 30 days.
Typically, the "Other" group
consisted of items that were causing
Node escalation
holds.
The
analysis techniques
used were essentially either
an "investigate
and
correct" or some form of a root cause analysis.
The inspector
reviewed the characterization
of selected
CRs.
The
inspector noted that many repetitive issues
were not assigned
root cause
evaluations.
Examples of these
are as follows:
CR 98-178 repeated
CR 97-383
CR 98-112 repeated
CR 96-2531
, CR 97-2301
was canceled
due to corrective actions
proposed for CR
97-2287
CR 97-1229 repeated
CRs 97-1091
and 97-395
These are discussed
in more detail in paragraph
07.6.
According to AP-0006130,
a
CR could be closed without completion of the
proposed corrective actions.
The proposed corrective actions were
entered into the
PMAI tracking program.
Control
and scheduling of PMAIs
were performed in accordance
with Administrative Procedure
AP-0006129.
Revision 7,
"PMAI Corrective Action Tracking Program."
The PMAIs
prioritization was based
on the
PNAI completion dates.
Most PMAI due
dates
were provided
by. the implementor.
Procedure
changes
or cr'eations
were not assigned
a due date but were requi red to be completed within 16
months with a priority for completion based
on the type of procedure
change.
Deficiencies related to the timely implementation of procedure
related
PMAIs are discussed
in Section 07.6.
The licensee
had several
different ways that
a
CR and the resultant actions could be classified.
The inspector
concluded that the actual significance of issues
could not
be easily determined
using the licensee's
method of characterizing all
issues
as Severity Levels requiring resolution in either
3 days,
10 days
or 30 days.
For example,
CR 98-'0029 documented that the security entry
12
gates did not always
open after the hand reader identified a person.
Occasionally,
the person
needed to reperform the entry procedure.
CR
98-0053 documented
a leaking Safety Injection Tank drain or fill valve
causing the Refueling Water Tank return header
and the Hot Leg Injection
return header
to pressurize.
Both of these
CRs were identified as
30
day severity levels.
Unless there
was
an operability or'reportability
concern
a 30 day Severity Level was assigned.
The inspector
reviewed the problem analysis for more than
100
CRs and
noted that the quality of the analyses
varied.
Among CRs
requi ring
root cause analysis,
those
CRs prepared
by individuals who had received
some form of root cause training were generally of better quality.
The
condition descriptions
for the
CRs reviewed were complete
and the cause
identified was supported
by facts gathered
during the investigation.
Conclusion
Problem identification was determined to be effective.
However,
repetitive issues
were not consistently
assigned
root cause evaluations.
The Severity Level designation
did not necessarily
indicate the actual
significance of the
CR.
Although the
PMAI process
was designed to
assign
due dates
based
on significance,
the inability to differentiate
significance
between
CRs hindered this process.
The inspector
considered this
a weakness- in prioritizing corrective actions for
identified problems.
Ade uac
of Corrective Action Pro
ram
Ins ection Sco
e
40500
The inspector
reviewed the most recent Quality Assurance
(QA) audits of
the,licensee's
Corrective Action Program
(CAP).
The inspector verified
that the scope
was adequate,
the investigation
was appropriate,
and the
conclusions
were well founded.
Additionally, the inspector
reviewed
seventeen
selected,
safety-significant Significant Condition Reports
(SCRs) for proper administration,
adequacy of analysis
and root cause
evaluations.
and appropriateness
of corrective actions.
Observations
and Findin s
The licensee's
QA organization
completed their audit QSL-CA-96-20,
"Corrective Action Functional Audit" on February
14,
1997.
The audit
identified eight findings that
QA stated indicated
a continuing weakness
in the corrective action program.
Overall. the inspector
found the
audit to be well performed.
The findings were documented with
substantiating
facts,
and the scope of the audit was appropriate.
The
weaknesses
identified by QA were limiting the effectiveness
of the CAP.
Section 07.6 discusses
further details of these findings and the
licensee's
attempt to correct these deficiencies.
The primary method of problem identification was the
CR.
As defined in
Administrative Procedure
AP-0006130.
Revision 12, "Condition .Reports,"
13
the program allowed any person working within the Florida
Power
8 Light
(FPL) Nuclear program to identify any problem or potential
problem to
the company, for resolution.
A subset of the
CR system
was the
system.
An SCR would be issued in response to a more serious condition
that would require
a higher level of management's
attention (for example
off-site notifications,
Emergency
Plan Activations, Technical
Specification required shutdowns, etc.).
The events that would require
an
SCR were defined in both AP-0006130
and ADM-17.02. Revision 13,
"Significant Condition Report Summaries."
The inspector
reviewed
17 safety significant SCRs.
The inspector
had
the following observations:
~
All SCRs reviewed
had been appropriately assigned
SCR status
as
defined by the licensee's'procedures.
~
The Root Cause
Evaluations for these
17
SCRs were assigned
according to Appendix 2 of AP-0006130.
~
Level'
Root Cause Analyses were well performed, well documented,
and appeared to identify all appropriate root and contributing
causes.
~
Overall.
Level
2 Root Cause Analyses were significantly less
formal.
The inspector
had difficulty in ascertaining if all root
causes
had been identified with a Level
2 Root Cause Analysis.
A
Level
2 Root Cause did not differ significantly from an
"Investigate
and Correct" analysis.
The licensee stated that they
had identified this and stopped
performing Level
2 Analyses.
~
All corrective
actions identified in SCRs were either completed or
properly tracked
by a PMAI;
~
All corrective actions
assigned
were appropriate, for the
identified root causes.
Also, the inspector
reviewed the licensee's
system to identify and
correct operator
workarounds.
The licensee actively tracked all
'orkarounds
via the
PMAI system.
At the time of the report the licensee
had seven
open items, all of which had been evaluated to correct.
Five
had work scheduled in the near future.
Periodically, the licensee
asked
the operators to reevaluate their job tasks
and determine if a
workaround might exist.
c.
Conclusions
The SCRs reviewed by the inspectors
were appropriately dispositioned.
The inspectors
noted
good Level
1 Root Cause Analyses
performed
by the
licensee's staff.
Lower grade evaluations
were noted to be mixed in
their quality.
Corrective actions
were appropriate for the identified
root causes
and the actions
were either completed
or transferred to
PMAIs before closing out the packages.
Additionally, the inspector
14
07.5
found the Operator
Workaround process effective in identifying and
correcting these deficiencies.
0 eratin
Ex erience
Pro ram
Ins ection Sco
e
40500
The inspector
reviewed the licensee's
Operating
Experience
Program,
and
evaluated the program's. effectiveness
in receiving, evaluating.
and
dispersing
information for use in the plant.
Observations
and Findin s
The inspector
reviewed the procedure
ADN-17.03. Revision 11, "Operating
Experience
Feedback" to determine the licensee's
requirements
for the
program.
The inspector
found the procedure to be general
in nature,
but
all requirements
were being met by the program.
.The inspector
reviewed the information that the Operating Experience
Administrator was putting into the corrective action program and found
that it was timely and usually beneficial.
The administrator
used the
personnel
resources
in the plant effectively to determine the
applicabi lity to the faci lity.
The inspector
noted that. typically, the
administrator
accessed
Part
21 notifications,
Information Notices.
Generic Letters
and industry information within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of issuance.
The information was processed
and filtered for usefulness
in a timely
manner.
In February
1997,
QA identified
a backlog of items from
December
1994 to Hay 1996 that had not been reviewed for applicability
or distributed to the plant.
This backlog had been worked off.
The inspector
reviewed
a sampling of the information forwarded to the
lant.
Generally, the appropriate divisions were given the information.
he division supervision further filtered the information and passed it
on to the worker level.
The workers felt that most of the information
was useful,
however, they also believed that there might be more
beneficial information available.
The workers interviewed believed that
the information reached
them in a timely fashion.
The inspectors
also
noted
a significant population of CR responses
included Operating
Experience information in them.
. Conclusions
The Operating
Experience
Program
was effective.
Information distributed
to the plant was generally timely and useful.
The backlog identified by
QA in 1997 had been worked off.
15
Self-Assessment
Ins ection Sco
e
40500
The inspector
reviewed the licensee's
selt-assessment
activities
including the site
QA assessment
activities.
Observations
and Findin s
Self-Assessment
A self-assessment
program was started at the site about two years
ago.
Administrative Procedure
ADH-11.05. Revision 0. "Self-Assessment
Procedure,"
provided the guidance for the self-assessment
program..
This
program required that each department
perform
a quarterly self-
assessment.
The inspector
reviewed the tracking and assessment
system
used
by the
program owner for self-assessments.
Nore recent self-assessments
were
assigned
a grade from zero to 100.
Each of the quarterly grades
was
tracked
by department.
The quality monitoring of the self-assessment
was self-critical.
Noteworthy was the review of a third quarter self-
assessment
done for fire protection which was given
a grade of only 20.
The assessment
was limited in that it only looked at emergency lighting
and did not assign corrective
action for the findings.
The inspector
concluded that this program was effective in providing feedback
on the
quality of the selt-assessments.
The inspector noted that the self-assessment
procedure did not require
an annual or periodic site-wide self-assessment.
The last site-wide
assessment
was performed in 1996.
No further site-wide assessment
was
planned at the time of the inspection.
~iit
A
The inspector
reviewed
an audit conducted
by QA of the site corrective
action program.
This audit started in October
1996 and was completed in
February
1997.
The inspector
reviewed the audit,
QSL-CA-96-20.
and
responses
to the audit.
This audit identified eight significant
noncompliances
with corrective action procedures.
The audit also
discussed
that stronger support of the corrective action mechanisms
must
be provided by the plant management
team at all levels.
The audit findings were:
CR reportabi lity review practices
were deficient in that failure
to identify two reportable conditions occurred.
Corrective Action processes
did not properly address
actions to
prevent recurrence of conditions adverse to quality.
16
Nonconformances
were not being evaluated
and classified
consistently in CRs.
h
A procedural
noncompliance
resulted in deficient review and
approval practices for corrective action documents
in a
significant number of cases.
~
A procedural
noncompliance
resulted in improperly validated
software being used to control
mode restriction items
on PHAIs
~
A lack of "attention to detail" resulted in corrective action
records containing insufficient detail to recreate
the actions
taken.
~
An ineffective management
of conditions
adverse to quality
resulted in delayed evaluations.
disposition,
and implementation
of corrective actions.
~
An effective Operating
Experience
Feedback
(OEF) Program
had not
been
implemented at St. Lucie.
This was
an effective
QA audit identifying substantive
issues with the
licensee's
corrective action program (CAP)., It should
be noted that
improvements to the
OEF Program were observed
and are discussed
in
section 07.5. of this report.
The inspector
also reviewed the
QA quarterly reports.
These reports
provided self-critical assessm'ents
and wer e used
as the basis
for the
site performance
windows report.
The windows report was
a one page.
color-coded display of the various departments'erformance
for several
quarters.
The
QA audits
and quarterly assessments
provided effective
self-critical reviews of plant activities.
However, during the review of many recent
CRs (1998), the inspector
found that the corrective actions for the previous
QA audit of the
corrective action program were not effective.
Correction of problems
was not timely and similar problems
found in the past
QA audit were
still occurring.
The corrective action program lacked focus
on timely
correction. and preventing repetition of previous problems.
Accordingly.
this was identified as
a violation of 10 CFR 50 Appendix B, Criterion
XVI, Corrective Action.
This violation was identified as
VIO 50-
335,389/98-06-03.
"Corrective Action Program
Lacks Focus
on Correction
of Problems",
and contained three examples.
Quality Assurance
documented in CR 98-0635 that
PMAIs issued
as
corrective actions for 29 procedure revisions
had been
open since
1996.
Further investigation
by the inspectors identified fifteen of the
Condition Reports
as potentially affecting the operation of safety-
related equipment.
Nine of those
CRs were determined .to be more than
"human factors" upgrades
and would add to the substance
of the
procedure.
These nine
CRs
(CR 96-1065,
96-1341.
96-1789,
96-1792,
96-
1865,
96-2065,
96-2189,
96-2311,
and 96-2768)
each
had at least
one
e
17
procedure
change related
PMAI outstanding.
The inspectors
reviewed,
in
detail, six of the nine
CRs (96-1065,
96-1789,
96-1792.
96-2065.
96-
2311,
and 96-2768),
and noted several
items of interest.
~
Every
PMAI issued in response to these
CRs was originally assigned
a due date before September
30,
1997.
Most were assigned
due
dates
before January
31,
1997.
The PMAIs were transferred to the
Procedures
Group in mid January
1997.
~
When transferred to the Procedures
Group, all of the
PMAIs were
. given
a priority of either
1 or 2.
These priorities superceded
the due dates.
However, the assigned priorities indicated that
the licensee did not believe that these
were the lowest level
priority procedure
changes.
~
One
CR (96-1792)
was dispositioned with a recommended
procedure
change to prevent
a loss of charging
and letdown during
maintenance.
Another
CR (96-2768)
was dispositioned with a
recommended
procedure
change to address
aligning the control
room
ventilation system following an auto start,
as described in the
FSAR.
The existing procedure did not agree with the
FSAR.
As of
the end of the report period, the changes
were still pending
issuance.
Criterion XVI of Appendix
B 'to 10 CFR 50 requi res the licensee to have
measures
"established to assure
.
.
. are
promptly identified and corrected."
On January
17,
1997,
Revision
5 of
procedure,
AP-0006129,
"PMAI Corrective Action Tracking Program."
added
a requirement for closure of all procedure
change related
PMAIs within
16-months.
Although the 16-month requirement to close
a procedure
was
not in place
when the subject
PMAIs were issued,
the licensee did not
properly track these corrective actions
and ensure
implementation
was
completed in a timely manner.
This is the first example of VIO 50-
335,389/98-06-03.
Quality Report 97-2271
and related
CR 98-0043 identified multiple CRs
with unsatisfactory
responses.
The
QA audit of 29
CRs found five CRs
inadequately dispositioned,
in that the corrective actions were not
adequate to correct the conditions.
This sampling of CRs indicated that
about one-sixth of CRs audited were unsatisfactory.
These issues
were
similar to a 1997 finding in QA Audit QSL-CA-.96-20 that was documented
in CR 97-282.
Although each of the individual
CRs were eventually
adequately dispositioned,
the licensee
had not yet fully address'ed
the
root causes
for the inadequate
dispositions.
The licensee
had failed to
ensure that
a significant condition adverse to quality (multiple
assignments
of inadequate
corrective actions to CRs)
was adeguately
corrected.
This is identified as the second
example of VIO 50-
335,389/98-06-03.
Additionally, Root Cause evaluations
were not -performed
as requi red by
site procedure.
Step 8.5.5 of AP-0006130,
stated that
a Root Cause
Analysis was requi red for those significant events listed in Appendix 6
18
of the same procedure.
Appendix 6 listed,
among other items,
inadequate
10 CFR 50.59 reviews/evaluations/screens.
QA Audit QSL-CA-96-20
identified multiple instances
of improperly assigned
problem analyses.
including examples
involving inadequate
50.59 reviews
and repetitive
equipment fai lures.
which were not investigated with a root cause
analysis
as required
by the licensee's
procedure.
The licensee's
response to the audit finding stated that Appendix 6 was provided as
guidance
and adherence
was not
a requirement.
It further stated that
a
certain
amount of human judgement
was involved in the assignment of an
evaluation level.
Since the audit,
QA identified in CR 98-043
a
condition in which a
10 CFR 50.59 screening
had not been performed
as.
required
by site procedures.
Likewise. the inspectors
i,dentified that
CR 98-0346 was written because
a Temporary System Alteration was
installed without a 10 CFR 50.59 screening.
Both .CR 98-043 and
CR 98-
0346 were not investigated with a root cause analysis
as required
by AP-
-0006130.
However,
NRC review of these
CRs verified that
a full 10 CFR 50.59 safety evaluation
was not required in either case.
Also.
NRC
regulations
do not require
a
10 CFR 50.59 screening.
Therefore,
the
inspectors
concluded that the lack of 50.59 screenings
in these
instances
was of minor significance
and is not subject to enforcement
action.
Additionally, the inspectors identified an example of a repeat
problem
concerning periodic procedure
reviews.
CR 96-2531 identified that 65
procedures
did not receive
a periodic review as required by QI-5-PSL-1,
Revision 7, "Preparation,
Revision, Review/Approval.0f Procedures".
and
Technical Specification 6.8.2.
CR 98-0112 again identified that
183
procedures
had not been reviewed
as required.
Appendix 6 of AP-0006130
required
a root cause evaluation to be performed for QA program
breakdowns,
such
as failure to follow verbatim compliance with
procedures.
Although this condition represented
a repetitive problem
resulting in a failure to implement the Quality Instruction,
a Root
Cause evaluation
was not identified as necessary
and was not performed.
The inspectors
concluded that these
examples
represented
multiple
failures by the licensee to perform Root Cause evaluations
as requi red
by the site procedure.
This is identified as the third example of the
VIO 50-335,389/98-06-03.
c.
Conclusions
The site self-assessment
program conducted quarterly and department
audits were of mixed quality.
Self-critical monitoring of these
assessments
was driving improvements in the process.
The site
QA audits
and quarterly reports provided self-critical reviews of plant
activities.
However. corrective actions for a
QA audit of Corrective
Action Program were not effective.
Recent
CRs dealing with
unsatisfactory
and untimely corrective actions were identified.
These
issues
were identified as
a corrective action violation.
19
On-Si te/Off-Si te
Commi ttees
Ins ection Sco
e
40500
The inspector
reviewed the on-site safety committee
and off-site
committee activities that were available during the period.
Observations
and Findin s
Off-Site
The inspector
reviewed the functions of the Company Nuclear
Review Board
(CNRB).
The requirements for the
CNRB are specified in TS 6.5.2.
The
inspector
reviewed the meeting minutes for meetings
440-451 covering the
time period of January
21,
1997. to January
29,
1998.
Each of the
meeting minutes indicated the members
and alternate
members
present.
Compliance with TS requirements for attendance
was verified.
The inspector
verified that required items were reviewed such
as safety
evaluations,
TS changes,
violations, Licensee
Event Reports
(LERs).
and
minutes of the Facility Review Group (FRG).
No deficiencies or problems
with TS compliance were identified.
Heeting
number
448 conducted
November 25,
1997,
addressed
the site plant
manager's
report and
a review of plant performance for 1997.
This
report reviewed
a 1996 site-wide self-assessment.
Weaknesses
were
identified and
a list of indicators tracked to determine the
.
effectiveness
of corrective actions for the weaknesses
was presented.
The inspector
reviewed this report and noted
an overall positive
improvement in plant performance.
This was evident by a declining trend
in the number of overdue
CRs, control
room instruments out-of-service,
reduction of backlogs,
and other items tracked.
The inspector
noted
a unique system termed the "ear ly warning
indicators."
The early warning system
was
a set of 25 indicators
used
as precursor indications of future plant performance.
These indicators
were monitored to enable early detection of negative
performance
so that
corrective actions
may be taken prior to experiencing
a significant
decline in plant performance.
The inspector noted that the overall
trend for the site was positive except for overtime hours.
This was
previously identified
a repeat
problem and an
NRC violation.
From the meeting minutes of the
CNRB, it was apparent that the reviews
conducted
were rigorous, challenging,
and conformed to TS requirements.
The use of early warning indicators
was
an enhancement
to the safety
review process.
On-Site
The inspector attended
an
FRG meeting
on April 14,
1998.
This meeting
focused
on the TS requi rement for FRG to review procedure revisions.
Thirty items were reviewed.and
one item was not approved.
The inspector
08
08.1
20
observed excellent
feedback to the sponsor of one procedure revision for
the quality of the 50.59 screening
review.
The inspector
reviewed compliance with the TS 6.5. 1 concerning the
requirements
for Facility Review Group
(FRG).
The quorum membership,
member disciplines,
meeting frequency,
and responsibilities
were
reviewed
and no problems
were identified.
FRG meeting minutes were
promptly available after the meeting.
The inspector
reviewed
FRG
minutes for meeting
number
98-088 held on April 14,
1998,
and
a follow-
up meeting,
number
98-090,
conducted April 15,
1998.
The follow-up
meeting
was held to approve
a change to the administrative procedure
AP-
0006130,
"Condition Reports," to transfer responsibility for CR review
and closure to line managers.
This change also deleted the requirement
to review CRs for repeat conditions.
This was done to provide
consistency
between the
FPL sites at the direction of senior management.
The inspector also reviewed recent guidance dated April 7,
1998.
entitled "Conduct of the FRG."
This guidance
reduced the
FRG membership
from 40 to 19 members in order to achieve consistency.
Also. noteworthy
guidance
was that each item presented
to FRG had
a sponsor.
The
FRG
chairman,
members,
and sponsor 's responsibilities
were specified
on
a
chart in the
FRG room.
This guidance
was seen
as enhancements
to the
process.
Conclusions
The off-site/on-site safety review groups provided an effective
oversight of TS required activities.
The use by the
CNRB of early
warning indicators
was
an innovative'approach
to detecting plant
problems.
Recent
changes
made to the
FRG meetings
were enhancements
to
their review process.
Hiscellaneous
Operations
Issues
Control
Element Assembl
Periodic Exercise
Ins ection Sco
e
61726
The inspector
observed portions of the performance of Procedure
OP 1-
0110050,
Revision 35, "Control Element Assembly Periodic Exercise."
Observations
and Findin s
On April 29, the inspector witnessed the Unit 1 Control
Room operators
exer cise seven
CEAs in accordance
with the aforementioned
procedure.
CEA movement
was actually performed by operators
in license training.
The activity was directed
by a licensed operator
and was overseen
by the
Assistant
Nuclear Plant Supervisor.
k
The inspector noted good use of three-part
communication
by the
participants.
The control
room was quiet with other activities kept to
a minimum during the surveillance.
The ANPS was noted to have provided
21
advice to the trainee
based
on personal
experience.
Overall control of
the evolution was considered to be excellent.
The inspector verified the procedure
was the proper revision and was
being adhered to.
Conclusions
The inspector considered
the operator performance of a surveillance
of
control element
assemblies
to be excellent.
The control
room was quiet
with little other activities or traffic.
Oversight of operators
in
training during this evolution was also excellent.
Conduct of Haintenance
II. Maintenance
Work Order Plannin
and Control Of Troubleshootin
Ourin
Maintenance
Ins ection Sco
e
62707
The inspector
reviewed
numerous
Work Orders
(WOs), focussing
on the
quality of planning. to verify that maintenance
troubleshooting
activities were being properly controlled and documented.
Additionally.
the associated
procedures
were also reviewed.
Observations
and Findin s
The inspector
reviewed the licensee's
procedure for the processing,
planning,
and working of WOs, ADN-0010432. Revision 18, "Control Of
Plant Work Orders."
In addition, the inspector
reviewed the licensee's
procedure for the control of maintenance
troubleshooting activities,
GMP-21 'evision 2, "Troubleshooting Process."
The inspector
randomly selected
eight
18C
WOs to review the level
and
adequacy of planning.
The inspector noted that seven of the
contained
a step to troubleshoot
and repair the associated
equipment.
The seven
WOs were;
9800495901,
9702586501,
9702112501,
9702619801,
9800347601,
9800499301
and 9702325101.
However,
none of the
contained the required troubleshooting
documents
requi red by GMP-21.
The approved planning of the
WOs would typically state
1) Investigate
the reported
problem.
2) Repair/Replace
as necessary
the affected
components.
3) If required, troubleshoot/repair
associated
components
as
directed
by supervision
using
GMP-21 and vendor technical
manuals
as
reference
as necessary.
The inspector
reviewed
GMP-21 and noted that it required
a formal step-
by-step troubleshooting
plan be developed,
however.
none of the
reviewed contained that documentation.
The inspector discussed this
issue with Maintenance
supervisors
who stated that
GMP-21 was not
actually used.
The step
was written into WOs as
a contingency to be
22
used if necessary.
The
WOs had been completed
as skill of the craft and
did not requi re the use of the documents
described in the
GNP.
The
licensee
provided several
examples of troubleshooting
WOs and the
inspector verified the appropriate
documents
were included in the
package.
The inspector concluded that GNP-21 was
an excellent tool in developing
work instructions for troubleshooting
equipment
problems.
The procedure
requi red
a logical sequence
of thought
and observation prior to actually
commencing work. It also provided for an adequate
amount of review and
oversight during the process.
One
WO reviewed
by the inspector,
9800499301,
written to rebuild the
plant vent stack sample
pumps,
contained only minimal instruction.
The
planning stated to remove the pumps from the skid and refurbish,
sending
it out to the vendor for rebuild if necessary.
Although the pumps were
safety-related,
the
WO contained
no guidance
on how to perform the
actual
refurbishment.
The inspector discussed this with the licensee
who stated that the planning was misleading.
The pumps did not get
refurbished,
but actually were replaced.
The
WO controlling this
activity was used to replace these
pumps
on
a regular basis
as part of a
,
preventive maintenance activity.
The practice of refurbishing the pumps
was discontinued
and the
WO was never revised.
The licensee
revised the
WO to more accurately reflect the maintenance activity.
The inspector
reviewed ADN-0010432, Revision 18, "Control Of Plant Work
Orders."
Step 7.3.2.0,
stated that "if a work task requires direction
beneath
the level of detail that is available with specific procedure or
technical
manual
guidance,
the work may be performed at the di rection of
and with direct oversight by the Maintenance Supervisor
(having
appropriate technical
assistance
when necessary)....."
Two restrictions
associated
with this step were:
1) Stay within the scope of the
WO or
'rite a scope
change,
and 2) Use GNP-21 when performing troubleshooting
activities.
The inspector discussed, the meaning of this step with
various maintenance
workers and supervision.
.A large percentage
of
workers interpreted this step
as providing authorization for work to be
conducted without a procedure
provided oversight
was provided by a
supervisor
.
The inspector noted that to do so would bypass the various
reviews necessary
to ensure the activity could be safely accomplished.
Additionally, work on equipment
such
as safety related,
seismic,
or fire
protection required
procedures
that had been reviewed by the Facility
Review Group.
The inspector
discussed this issue with Haintenance
supervision
who
stated that the intent of the step
was to limit the work accomplished
at
the direction of the supervisor to minor maintenance
or skill of,the
craft activities.
The licensee
revised the step in Revision
20 of the
procedure.
The inspector
concluded that
a large portion of ISC work, by its very
nature,
involved troubleshooting.
It was
a routine practice to plan
with a heavy reliance
on skill of the craft and supervisory oversight.
23
WOs were written to include
a step to allow troubleshooting, if needed.
However, the inspector
found few examples
where it was used.
The
troubleshooting activities were generally determined
by the maintenance
worker in the field and his supervisor
as the job progressed
and were
considered skill of the craft.
In the cases that were considered
beyond
skill of the craft, written instructions
were provided.
The inspector
did not identify any examples of work which had been performed
inappropriately.
Conclusions
The inspector concluded that the licensee's
method of WO planning was
adequate.
but placed
a heavy reliance
on the skill of the maintenance
worker and supervisory oversight.
The inspector did not identify
examples
where this reliance resulted in inadequate
work.
In addition,
the inspector
concluded that GAP-21 provided
an excellent tool
developing work instructions
and controlling troubleshooting of
equipment
problems.
En ineered
Safe uards
Rela
Test
Unit 2
Ins ection Sco
e
62707
The inspector
observed portions of OP 2-0400053,
Revision 27.
"Engineered
Safeguards
Relay Test."
Discussions
were held with
maintenance
workers, control
room operators,
and supervisors.
Observations
and Findin s
The inspector
observed the preparation
and set-up for the performance of
Safety Injection Actuation Signal,
Containment Isolation Actuation
Signal,
and Containment
Spray Actuation System
Channel
A, Group
2
testing.
The inspector
reviewed the procedure in use by the maintenance
workers
and found it to be the correct procedure
and the current
revision.
The knowledge level of the operations
personnel
and
technicians with regard to the procedures
was verified by the inspector
through questioning
and found to be good.
While the
I&C technicians
were performing
a dry run to verify and label
all terminal
board test points,
a discrepancy
was found in the
procedure.
The technicians
found the discrepancy
as
'a result of the'ry
run while .comparing the terminal
board wiring with the drawings
and
procedure.
The procedure,
a first time use procedure,
incorrectly
identified
a terminal board test point location.
The licensee
backed
out of the procedure
so that
a temporary change
(TC) could be made to
the procedure prior to continuing with that portion of testing.
The
inspector
observed
the. performance of the restoration
and verification
steps
by operations
personnel
and found it to be performed properly.
While observing the test.
the inspector identified a void in the fire
barrier on the control
room floor inside the east
"SA" safeguards
0
M2
H2.1
24
E
cabinet.
The inspector could not see if the void extended
completely
through the floor.
This void was brought to the attention of the
licensee.
A fire breach permit was initiated and
CR 98-0723 generated.
The licensee will determine the extent of degradation of the fire
barrier during the next outage of sufficient duration to de-energize
the
cabinet.
Conclusions
The experience
and thoroughness
of the maintenance
and operations
personnel
helped identify a procedural error involving the testing of
safety components.
The inspector
concluded that the correct actions
were taken when the error
was identified.
The actions that were taken
were properly performed.
Maintenance
and Material Condition of Facilities and Equipment
4
Safet
Related
Recorder
Maintenance
Ins ection Sco
e
62707
The inspector
reviewed the maintenance
history of multiple safety-
related recorders for the time period July 1,
1997 through April 30,
1998.
The inspector
reviewed the records for common failures and
problems, timely repai rs,
and documentation of work.
Observations
and Findin s
The inspector
reviewed greater than
100 safety-related
work orders for
control
room chart recorders.
The vast majority of these
work orders
were preventive maintenance
(PH) items
as prescribed
by the various
recorder's
Technical
Manuals
and as described
by the applicable
18C
rocedure.
Any recorder that provided an indication required
by
echnical, Specifications
(TS) was clearly identified within the work
scope
as being
a
TS required instrument.
For example,
which would perform the midpoint calibration check for the
Flow Indication, identified this
PH as partially
satisfying
The inspector identified no problems with the
PH
documentation.
The inspect'or also reviewed approximately twenty work orders identified
as "Trouble and Breakdown."
Nearly all these
work orders
were performed
to correct
a recorder failing to advance,
a recorder
spiking,
a recorder
indication fai ling to change.
or a recorder fai ling to ink.
The
inspector identified no clear,
recurring problems with any individual
recorders.
Parts
were available for recorder
repair within a few weeks.
However, several
maintenance
workers
and work control personnel
did note
that the age of the recorders
was making parts
replacement
more
difficult with time.
The inspector did note that.
on average.
the licensee
would fix the
safety-related
recorders
four to six weeks after
a problem was
25
identified.
Conversations
between
personnel
in Work Control
and the
inspector
suggested
that this was expected.
The licensee
has
adopted
a
thirteen-week
maintenance
schedule.
Administrative Procedure
ADM-
0010432.
Revision 18, "Control of Plant Work Orders"
ranked work based
on the plant's
needs.
Emergency
Work was classified
as work that must
be started
immediately.
Examples of this type of work were the
following:
TS 3.0.3 related fai lures
Unidentified steam or through wall leaks
Unplanned unit load threats
Potential for major equipment
damage
Degrading equipment condition with the potential for
significant consequences
The next level of significance included work that should
be started
within two weeks.
This category included the following:
~
A severe threat to personnel
safety
~
An actual
load limit greater than one megawatt
~
Event Response
Team support
~
TS Limiting Conditions for Operation with a unit shutdown in
less than
72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br /> or
NRC notification
~
Control
Room nuisance
alarms
~ 'lant General
Manager Directive
The third level of work would be performed
between
two and seven
weeks.
Examples of this type of work included:
~
A worsening condition affecting component operability
~
Equipment
needed
regardless
of system work week
~
A condition adverse to Maintenance
Rule availability impact
~
Drip pockets
~
Control
Room deficiency tags
All other work would be scheduled after seven
weeks.
The inspector
discussed
these procedural
requirements
with Work Controls
personnel
and questioned
the advisability of delaying work on safety-
related
equipment.
The licensee
asserted
that this plan met all
regulatory requi rements,
allowed proper prioritization of work. and
allowed efficient use of thei r maintenance
workers.
c.
Conclusions
The inspector concluded the safety-related
recorder
maintenance
program
was able to maintain the equipment operable despite the aging of the
recorders.
Finding replacement
parts for these
recorders
has not yet
impacted the program.
The licensee
was following their program to
schedule repair of non-functioning recorders.
26
Miscellaneous
Maintenance
Issues
Closed
VIO 50-389/97-05-01
"Fai lure To Control Forei
n Material
Enterin
and Exitin
The Unit 2 Containment-
92902
This violation occurred
as
a result of not controlling the Unit 2
containment
as
(FNE) area
as required
by
procedure.
An inspection identified incomplete logs of equipment taken
into and out of containment.
As a result of the violation the licensee
completely revised the controlling procedure,
QI 13-PR/PSL-2,
"Foreign
Material Control, Housekeeping
And Cleanliness
Control Methods."
The
inspector
reviewed Revision 35 of that procedure
and noted
much more
stringent controls of foreign material.
In addition, the licensee
developed
pamphlets
which describe the process,
posted signs throughout
the plant to serve
as reminders
about the program,
and provided training
to personnel
that might be involved with FNE (i.e. maintenance
workers,
utility men and operators).
The licensee
also revised HPP-l, "Radiation Work Permits."
Form 1.4,
'hich
is used to control containment entries in Modes 1, 2,
3 and 4 when
no work is to be performed.
The inspector verified the change
had been
incorporated into the current revision,
Revision 11.
In addition, the
licensee prohibited the use of the unit restart
open items list as
a
method for controlling FNE in the containment.
The inspector
reviewed
AP 0010728,
Revision 23, "Unit Restar't
Readiness,"
and verified that
this change
had been
made.
The inspector considered
these actions
adequate to prevent recurrence.
This violation is closed.
Conduct of Engineering
III. En ineerin
Generic Letter
Safet
Related
Motor 0 crated
Valve Testin
and Surveillance
Pro ram
Im lementation
Ins ection Sco
e
Tem orar
Instruction 2515-109
The objectives of this inspection were to review:
1) the licensee's
response to
NRC Integrated
Inspection
Report (IR) 50-335,389/97-11,
and 2) the Motor Operated
Valve (NOV) program implemented in response to
The inspection
was conducted through reviews of documentation
and interviews with licensee
personnel.
Observations
and Findin s
Guidance for the
NOV program was documented in Florida Power and Light
(FPL) Procedure
JPN-PSL-SENP-91-030,
"St. Lucie Plant Units
1
8
2
NRC Generic Letter 89-10 Program Description," Revision 6, dated October 22,
1997.
Specific engineering
documents
contained the justifications for
J
0
27
MOV program assumptions.
These included justifications for valve
factors,
load sensitive behavior,
and stem friction coefficient
assumptions.
Inspection
Report 97-11 and the licensee's letter (Letter L-97-258)
dated October
10,
1997, identified 13 issues
and the associated
corrective actions
needed to resolve the Nuclear
Regulatory
Commission
(NRC)'s concerns with the
NOV program.
The following sections
discuss
these
13 issues.
(1)
Weak Valve Factor Justifications:
IR 97-11 identified several
weak
valve factor justifications.
In its October
10,
1997 letter, the
licensee
committed to take the following specific actions to
resolve these
concerns.
~
Closed
Grou in
Criteria - The licensee's
grouping criteria
had not considered
a valve's American Nuclear Standards
Institute pressure
class or the system's fluid temperature.
The
inspectors
reviewed JPN-PSL-SENP-94-027.
"St. Lucie Unit 1-
Motor Operated
Gate.
Globe,
and Butterfly Valve Grouping for NOV
Dynamic Test Reduction
Program," Revision 5, dated
March 30,
1998 and JPN-PSL-SEMP-95-024,
"St. Lucie Unit 2 - Motor Operated
Gate.
Globe.
and Butterfly Valve Grouping f'r MOV Dynamic Test
Reduction Program," Revision 3, dated
March 30.
1998.
The
procedures
had been revised to include the above criteria and to
regroup the
NOV valve population.
This item is closed.
~
Closed
Inade uate 0 en Valve Factor Data for Valves 1-V3206
1-V3207
1-V3452
1-V3456
and 1-V3457
- The original valve
factor justification for this group did not include open dynamic
test data to address
performance in the open safety function
di rection.
The inspectors
reviewed the dynamic tests of valves
in this group which were reanalyzed
using Electric Power
Research
Institute (EPRI)'s extrapolation criteria and concluded
three tests
had adequate
disc loading levels to provide reliable
open valve factor information which was used to justify the
valve factors
used
by this group.
This item is closed.
~
Closed
Low Differential Pressure
Test Conditions for Valves 1-
MV-08-1A/B - These valves were originally tested at very low
differential pressures
relative to a design-basis
differential
pressure of 1015 psid.
The licensee recently retested
these
valves
and was able to obtain significantly higher differential
pressure
conditions.
The inspectors
reviewed the test results
which demonstrated
that the valves were flow-over-the-seat
globe
valves
and were self-closing in their safety function direction.
This item is closed.
~
Closed
Address
Unwed in
for Valves 'MV-09-9
'NV-09-10
MV-09-11
and ~r-MV-09-12 - These
WKN balanced-plug
had not been analyzed to determine whether significant. unwedging
loads could exist under design-basis
conditions.
Several
near
28
'design-basis
dynamic test results
were reviewed by the
inspectors
and no unwedging concerns
were observed.
Dynamic
testing of this valve design will continue
as part of the long-
term
NOV program.
This item is closed.
~
0 en
Inade uate Close Valve Factor s for Valves 2-NV-08-12/13-
The licensee
was unable to perform meaningful
dynamic tests
on
these
4 inch Anchor/Darling double-disc"gate
valves in the close
direction.
To justify the applied valve factors,
the licensee
compared
EPRI Performance
Prediction Methodology
(PPN) flow
isolation model results to the results obtained
from the
industry standard
equation using
a 0.50 valve factor.
This
comparison
found that the industry standard
method bounded the
PPH results
and was used
as the basis for continued
use of a
0.50 valve factor .
The inspectors
observed that these Auxiliary Feedwater
(AFW)
Pump Steam Supply valves
have
a design-basis
function to close
under high-energy line beak conditions.
Therefore,
some
additional
stem thrust,
beyond flow isolation, is necessary
to
ensure that these
valves continue to meet thei r safety function
under all.plant conditions.
A new
PPN calculation
was performed that
assumed
the worst-case
lower wedge orientation,
so that
a bounding prediction could be
established.
The current torque switch settings
were found to
be approximately
midway between the current
minimum required
thrust
and the worst-case
PPM prediction for full disc wedging.
This provided confidence that the valves would reliably perform
thei r safety function at their cur rent settings.
Further, the
licensee will increase
actuator capability during the upcoming
Unit 2 outage.
The licensee
issued Plant Manager Action Item
(PNAI) PN 98-04-072 to revise program documents
and thrust
calculations to establish
a minimum thrust requirement that
ensures
adequate
mechanical
wedging of the valve discs
under
design-basis
conditions.
~
Closed
Inade uate Close Valve Factor
for Valves 2-V3481 arid 2-
V3651 - The licensee
reviewed the design-basis
conditions for
these
valves
and determined that they were not closed under
differential pressure
conditions.
Therefore.
the close valve
factor
does not affect the close thrust requirements
for these
valves.
The inspectors
agreed with this determination.
'This
item is closed.
~
0 en
Inade uate Close
Mar in for Valves 2-HV-08-1A/B - Unit
2's Hain Steam Isolation Valves
(MSIV) bypass
valves were found
to have inadequate
actuator capability to meet their close
safety function and were declared
The licensee
de-
energized
these valves in their close safety function position.
PMAI PM97-10-113
and modification package
PC/H 98014 had been
issued to implement actions to increase
the margin for these
29
valves.
Further, the valves will be reversed to change the flow
direction across
the valve plug.
These modifications were
scheduled to be implemented during the Fall
1998 Unit 2
refueling outage.
~
Closed
Justif
Safet
Function for Valve 2-MV-08-3 - AFW
Turbine Tri
Throttle Valve - The licensee
reviewed the safety
function for valve 2-MV-08-3 to ensure that it was correctly
classified
as not having an open safety function.
Condition
Report
(CR) 98-0457
documented the licensee's
review of the
Final Safety Analysis Report
and the emergency operating
procedures.
This review determined that 2-MV-08-3 is maintained
in its open safety position and is,not relied upon to re-open
after
a turbine overspeed trip because
the accident analysis
relies
on the 2 motor-driven
AFM pumps.
Additionally,
Operations
personnel
confirmed that this understanding
was
consistent with plant operating procedures.
This item is
closed.
~
Closed
Inade uate Close
Mar in for Valves 2-V3550
2-V3551
and 2-V3536 - Globe valves 2-V3550,
2-V3551,
and 2-V3536 were
found to have inadequate
actuator capability to meet their close
safety function.
The licensee
revised 2-V3536's thrust
calculation to take credit for its flow-over -the-seat
design
which assists
closure of the valve.
This removed
any capability
concerns
for this valve.
Further review of the design-basis
requirements
for valves
2-V3550 and 2-V3551 identified that
these valves
do not have
a close safety function.
This item is
closed.
(2)
Closed
Periodic Verification Plan Did Not Address
D namic Te tin
of Globe Valves:
The licensee's
periodic verification program was
described
in PSL-ENG-SEMS-97-018,
"Periodic Verification of Design
Basis Capability of Safety Related
Motor Operated
Valves for NRC Generic Letter 96-05", Revision 3, dated -April 9,
1998.
. Inspection Report 97-11 identified that dynamic testing of globe
valves
was specifically excluded.
In its October
10,
1997 letter
.
the licensee
committed to revise the program to include dynamic
testing of a sample of balanced disc globe valves.
The inspectors
verified that these
changes
were implemented.
However, the
inspectors
noted that the licensee did not intend to dynamically
test
any unbalanced
The licensee's
decision
was
based
on
a preliminary assessment,
as part of the Joint Owners
Group
(JOG) program on
MOV periodic verification. that unbalanced
globe valves were not susceptible to degradation
mechanisms.
The
inspectors
indicated that the
JOG is now including some unbalanced
globe valves in their test program to validate this assumption.
In
response,
the licensee
revised
PSL-ENG-SEMS-97-018 to include
a
review of the JOG's
unbalanced
globe valve testing
and to reassess
the need to perform continued testing of unbalanced
if necessary.
This item is closed.
T
30
(3)
(4)
(5)
(6)
(7)
Closed
Globe Valve Calculations
Did Not Use Correct Disc Area
The inspectors
reviewed Mechanical
Standard,
STD-H-003,
"Engineering Guidelines for Sizing
8 Evaluation of Limitorque Motor
Operators,"
Revision 3, dated 10/31/97.
which had been revised to
rovide guidance
on determining if globe valves were guide or seat
ased for PPH calculations.
Additionally, the inspectors
reviewed
PSL-1FJH-91-019.
Revision 12,
and PSL-2FJM-91-048,
Revision 12,
which had been revised to identify which globe valves were guide
based.
This item is closed.
Closed
D namic Testin
Data Extra olation Guidance
Needs
~Udatin:
The licensee's
justification for linear extrapolation of
dynamic test data did not include EPRI's latest
recommendations
for
identifying the disk loads that were necessary to ensure that test
results
were reliable for extrapolation.
Licensee
personnel
had
revised
JPN-PSL-SEMP-91-030
and their linear extrapolation
justification to include.EPRI's extrapolation criteria.
A review
of previous extrapolations
using this guidance
found that all
existing dynamic test conditions were adequate.
This item is
closed.
Closed
Condition
Re ort 97-1732
Does Not Address
Load Sensitive
Behavior in the 0 en Direction:
Condition Report
(CR) 97-1732
determined that the original 10.5 percent
load sensitive behavior
margin was non-conservative.
Analysis of in-plant data using
methods
determined that
a, 22.5 percent
margin was appropriate.
However,
CR-97-1732 did not specify
a margin'or the open
direction.
To resolve this issue,
the licensee
revised the open
setup calculations to include the 22.5 percent margin.
CR 97-1734,
Supplement
1, addressed
the revised margins
and identified 3 valves
that required further review (1-V2514, 2-V3663,
and 2-V3665).
These valves were found acceptable
based
on valve-specific dynamic
test data.
This item is closed.
Closed
Revisions
Needed to Address Effects of Stem Lubricant
Chan
e on Stem Friction Coefficient and
Load Sensitive
Behavior
The licensee recently changed the standard
stem lubricant from
FelPro
N5000 to Mobil 28 which may have different performance
characteristics,
The licensee will monitor for stem friction
coefficient and load sensitive
behavior
performance
changes
as part
of the long term
MOV program.
Load sensitive behavior
and stem
friction coefficient justifications will be revised to reflect the
new test data,
as necessary.
This item is closed.
Closed
No Mar in Identified for
A e Related
De radation:
The
licensee
had not identified
a margin for valve degradations.
PSL-
ENG-97-018,
"Periodic Verification of'esign Basis Capability of
Safety Related Motor Operated
Valves for NRC Generic Letter 96-05,"
Revision 2, dated 4/3/98,
was revised to include
a minimum 10
percent thrust margin goal.
The licensee
also
had identified 48
MOVs that will be modified over the next three outage cycles to
attain this margin goal.
This item is closed.
31
(8) 'losed
MOV Calculations
Need to Be
U dated to Incor orate the
Latest
Desi
n Information: The inspector
reviewed PSL-lFJH-91-017.
Revision 12; PSL-2FJN-91-048,
Revision 12;
Revision 3;
and L-MECH-CALC-017, Revision 4.
These procedures'ad
been revised to address
non-conservative
valve factors,
load
sensitive behavior,
and include
PPH results for non-testable
valves.
This item is closed.
(9)
Lon
Term Plans
Where
PPH is Considered
"Best Available Data:"
Engineering
Report JPN-PSL-SENS-96-070,
"Evaluation of EPRI
HOV
Performance
Prediction
Program Results,-
NPR Report 1759," Revision
3. dated
March 30,
1998, describes
how the
PPN is applied to MOVs
and identifies several
cases
where the conditions for model
application were not met.
These results
were considered to be
"best available data."
In its October
10,
1997 letter, the
licensee
committed to develop plans to resolve
each of these
cases.
The licensee's
actions to implement these
plans are discussed
below.
~
0 en
Nona
licable Guide and Seat Material Combination-
EPRI's
PPH was not validated for valves that use Deloro on the
guide and disc seating surfaces.
Valve 1-V3480 (10 inch Velan
gate valve) uses .this material.
A contractor study showing
Deloro and Stellite 6 .as haying similar friction characteristics
was used
as
an interim justification.
Further
. the
JOG program
test plan includes at least
one valve that has Deloro internal
surfaces.
The licensee
issued
PMAI PH98-04-071 to monitor the
JOG and other industry testing
and to compare this information
to
PPN predictions
as
a long-term resolution of this issue.
~
Closed
Nona
licable Butterfl
Valve Bearin
Material-
Butterfly valves
~g-NV-07-ZA/B, 2-NV-'14-3, and Z-HV-14-4 were
identified to use
a nylatron bearing material that was not
included
as part of the
PPH validation program.
The licensee
reviewed existing dynamic tests for valves
1-HV-07-2A/B using
EPRI methods to measure
the bearing friction coefficient.
This
testing resulted in a bounding coefficient of friction of 0.,26.
For conservatism,
a coefficient of 0.35 was used
by the
PPN
prediction.
In-plant investigations
found that valves 2-NV-07-
2A/B have bronze bearings.
Therefore,
the
PPH predictions are
directly applicable to these valves.
.The bearing material
concern
was resolved for valves
2-NV-14-3 and 2-MV-14-'4 as they
have'no safety function in either di rection and were removed
from the
GL 89-10 program.
This item is closed.
~
0 en
Com ressible
Flow Globe Valves
- The licensee
applied
results to the HSIV bypass
valves
(2-NV-08-1A/B) which are globe
valves that operate
under steam
(compressible
flow) conditions.
Engineering
Report JPN-PSL-SEHS-96-070
noted that the
PPN is not
validated for globe valves that are in compressible
flow
applications.
The licensee
issued
PMAI PH97-10-133
and
modification P/CN 98014 to modify these
valves to increase their
32
(10)
margin dur ing the Fall
1998 Unit 2 refueling outage.
Further,
dynamic tests will be performed to establish
design-basis
settings.
~
0 en
Inverted Valve Guides
- Valves 1-HV-15-1 and 1-MV-18-1
use
an inverted guide design.
where the guide rai 1 is part of
the valve disc which rides in a slot in the valve body.
The
was not validated for valves with this design.
A contractor
study was used to justify use of the
PPH as "best available
data."
This study modified the guide offset dimensions
used
by
the
PPH and determined that disc tilting and nonpredictable
behavior
was not
a concern for these valves.
Engineering
Report
JPN-PSL-SEMS-96-070
stated that industry test
programs would be
monitored
and
new information would be incorporated
as it
becomes available.
The licensee
issued
PMAI PH98-04-71 to
communicate with industry sources
and other licensees to
identify existing
or future testing of this valve design.
Closed
Non redictable
Behavior
- The
PPH results for valves 1-
MV-09-7/8 originally determined that these
valves would be
nonpredictable
due to disc tilting and the sharp disc, seat
ring, and guide edges
assumed
by the
PPH.
These valves were
subsequently
opened,
and the seat
and guide edges
were verified
to be rounded in accordance
with EPRI's criteria.
Revised
PPH
calculations
resulted in a predictable thrust requirement
and
resolved this
PPH applicability issue.
This item is closed.
~
0 en
Valves Sizes
Lar er than
18 Inches
- The licensee
had
applied
PPM results to several
20 inch gate valves
(1-MV-09-1.
1-MV-09-2. 1-HV-09-7. and 1-HV-09-8).
The
NRC safety evaluation
(dated
Harch 15,
1996)
on the
PPH indicated that the
PPH
was validated for specific solid and flex-wedge gate valve
design
up to 18 inches in size.
Engineering
Report JPN-PSL-
SEMS-96-070 stated that industry test programs
would be
monitored
and new information would be incorporated
as it
becomes
available. Additionally, EPRI will be contacted to
determine the status of EPRI's efforts to validate the gate
valve model for valves in excess of 18 inches.
The licensee
issued
PMAI PM98-04-71 to track this validation effort. The
licensee's
MOV periodic verification program requires that
a
post-outage
report be completed within 3 months of the end of a
refueling outage.
The licensee
intends to use this report to
update its efforts taken to complete the actions identified in
the
PMAIs.
Closed
U date Total
E ui ment Oatabase:
The inspectors
reviewed the Total
Equipment
Oatabase to ensure that it had been
updated.
This review consisted of a sampling of ten percent of
the
GL 89-10 valves.
Findings were acceptable
and this item is
closed.
(12)
(13)
33
Closed
Plans to
U
rade
Low Mar in Valves:
PSL-ENG-97-018
was
revised,
as noted
above in Issue 7, to include
a minimum 10
percent thrust margin goal.
The licensee identified 48 HOVs
that will be modified over the next three outage cycles to
attain this margin goal.
This item is closed.
Closed
Use of Stem Friction Coefficients
Less Than 0.20:
The
licensee's
stem friction coefficient study analyzed gate
and
globe valve data points obtained
from static testing
and
justified a 0.20 stem friction coefficient for valves.
However,
IR 97-11 identified that
a 0. 15 stem friction coefficient had
been
assumed for valves 1-HV-09-1. 1-MV-09-2, 1-HV-09-7, and
1-HV-09-8.
The setup calculations
used
a 22.5 percent thrust
margin to account for load sensitive behavior.
These valves are
scheduled for future margin improvements
and stem friction
coefficient performance will be monitored each outage until the
modifications are complete.
for valves
2-V1476 and 2-V1477,
Power Operated Relief Valves
(PORV) Block
valves,
were reviewed.
These
assessments
used
a stem friction
coefficient of 0
~ 15 based
on valve-specific static testing where
the results
were less than 0. 15.
This item is closed.
0 en
PORV Block Valve Lon
Term Plan:
IR 97-11 .identified
margin concerns for the Units
1 5 2
PORV Block Valves (1-V1403.
1-V1405.
2-V1476,
and 2-V1477).
Valve 1-V1403 was closed
and
declared
inoperable for the closi.ng stroke in accordance
with
Technical Specification Limiting Condition for Operation 3.4. 12,
which requires the valve to be closed
and power removed.
In its
October
10,
1997 letter, the licensee
committed to make the
following changes to Unit 1's
PORV Block Valves during the
January
1998 refueling outage:
1) change the valve stem material
to eliminate the potential for stem embrittlement,
2) replace
the valve disc with one that has stellited guide slots,
and 3)
increase
the available thrust margin.
The inspectors verified
that the modifications were implemented,
including stem and disc
replacement
and rounding of disc and guide edges
as documented
in JPN-PSL-SEHP-96-070.
An actuator gear change
was
made to
increase
actuator capacity.
The Unit 1
PORV Block Valves now
have
25 percent
margin based
on use of actuator pullout
efficiencies
and
a 0.2 stem friction coefficient assumption.
The licensee
also committed to assess
the Unit 2
PORV Block
Valves (2-V1476,
and 2-V1477) margins to determine if
modifications are needed.
These valves currently rely on
that use actuator
run efficiency and
a
0. 15 stem friction coefficient assumption.
Modification Package
PC/H 98013 identifies actions that will increase
these
valves'argins.
These modifications were being tracked
by PMAI PH97-
10-115
and were scheduled to be implemented during the Fall
1998
Unit 2 refueling outage.
34
E2
E2. 1
Other
Issues
The licensee's
grouping method identified a "prototype" valve for each
group which contained valves that were testable
under dynamic
conditions.
This "prototype" valve was based
on its available margin
and risk significance.
The licensee's
program specified that only a
given group's "prototype" valve be considered for future dynamic testing.
in conjunction with the
JOG effort to address
periodic verification of
MOV switch settings.
The inspectors
noted that dynamic performance
information will be needed for any valve group that is not covered
by
the
JOG program.
The licensee
agreed to include this consideration
as
part of the long-term
MOV program.
Conclusions
The
NRC staff review of the
GL 89-10 program at St. Lucie is being
closed
based
on the completed
and scheduled
work, including the actions
identified in the
PMAIs noted above.
The completion of the commitments
in the
PMAIs and the closure of the specific remaining items described
above will be tracked
as Inspection Follow-up Item. IFI 50-335.389/98-
06-04,
"Completion of'otor Operated
Valve. Program Follow-up Items."
Engineering Support of Facilities and Equipment
En ineerin
Su
ort of Sodium
H droxide Tank Issues
Ins ection Sco
e
37551
On April 8, the licensee identified that the Unit 1 Sodium Hydroxide
(NaOH) Tank level indication was off-scale high,
and Operations
was
unable to verify that level was less than the maximum amount allowed by
Technical Specifications.
The inspector noticed that this was the
second. problem identified with NaOH tank level in two months.
The
inspector
reviewed Engineering's
disposition of both Condition Reports
(CR) for adequacy of the corrective actions
and depth of condition
review.
Observations
and Findin s
On February 9, Chemistry noted in Condition Report
CR 98-0214 that the
level indication on the Unit 1
NaOH tank did not correlate with the
'olume
of NaOH added
and drained from the tank as calculated
using the
strapping tables.
The System
and Component Engineer's
(SCE) response to
the
CR reviewed the history of the
NaOH tank.
A 1985 change
lowered the
required flow rate,
changed the weight requirement of the
NaOH,
and
changed the level requirements
in the tank.
The maximum allowable level
in the tank was then greater than the maximum indicated level.
The
evaluation continued
by describing
how the minimum volume would be
ensured
by low level alarms.
If level
was maintained on-scale,
the
maximum level would not be exceeded.
35
The
CR response
did not specifically address
the fact that several
. iterations of adding
and removing
NaOH did not cause the observed
level
changes to be as expected.
The
CR response.
however, initiated two
corrective actions.
First, the level instrument
was scheduled for a
calibration.
The engineer believed that an out-of-calibration
instrument could have been the cause of the mismatch.
Second.
the
issued
a
PMAI to issue
a Request for Engineering Action to change the
range of the level instrument or identify precautions to prevent the
tank level from exceeding the top of the indicating band.
Three weeks after the
CR response
was issued,
18C performed
a
calibration check
on the instrument.
They found that the instrument
was
within all tolerances.
The ANPS determined that no further work was
required
on the instrument.
This information was not fed back to.
Chemistry or the
SCE for resolution
or further investigation.
This lack
of feed back is identified as
a weakness.
Approximately one week later, Operations
found the level in the
NaOH
tank greater than
80 inches
(top of indicating range).
The licensee
conservatively. entered
a 72-hour shutdown Action Statement for Technical Specification (TS) 3.6.2.2 since they were unable to confirm that the
contained
volume was less than
5000 gallons.
Also. the licensee
was
uncertain that the concentration
had not been diluted out of
specification.
The licensee's
immediate actions
included draining the
tank into the gage
range
and verifying the
NaOH concentration.
Based
upon the amount of NaOH drained.
the
SCE confirmed that the level never
exceeded
the TS limits.
Chemistry results confirmed that the
concentration
remained within the
TS limits.
CR 98-0612,
was issued to determine the cause of the level increase.
The
SCE identified two potential
leak paths,
the nitrogen supply lines
or the closed solenoid valves to the containment
spray system.
The
had identified a constant
level increase of 0. 1 inches per five day
period.
Recently,
the licensee
had completed maintenance
on the nitrogen
supply line valve and had seen
no indication of water intrusion.
The
SCE planned to evaluate the other possibility during the quarterly
stroke test of the solenoid valves in May.
Approximately one week later, Operations
found the level in the
NaOH
tank greater than 80 inches
(top of indicating range).
The licensee's
immediate actions included draining the tank into the gage
range
and
verifying the
NaOH concentration.
CR 98-0612
was issued to determine
the cause of the level increase.
The
SCE identified two potenti'al
leak
paths;
the nitrogen supply lines or the closed solenoid valves to the
containment
spray system.
The
SCE had identified a constant
level
increase of O.l inches per five day period.
Recently,
the licensee
had
completed
maintenance
on the nitrogen supply line valve and had seen
no
indication of water intrusion.
The
SCE planned to evaluate the other
possibility during the quarterly .stroke test of the solenoid valves in
May.
36
The inspector discussed
the issues with the
SCE including the intent of
the original
CR, 98-0214.
The
SCE verified that the strapping tables
'ere
adequate
by reviewing the calculations in PC/M 231-177.
The
was confident that he understood the problems with the level
indications.
He also acknowledged that there
had been
a missed
connection with I&C's and Operation's
handling of the calibration
discussed
above.
The inspector learned that the
SCE had discussed
the
issues
concerning the tank and its level indication problem with the
Chemistry Supervisor
and they were working to get
an acceptable
solution
in place.
Conclusions
Upon identification, the
SCE actively worked toward correcting
deficiencies with the
NaOH tank level indication.
The inspector noted
good communications
between the
SCE and Chemistry in determining the
problem and corrective actions.
A weakness
was identified when
Operations
and
18C failed to inform Chemistry or the
SCE about the
results of work performed
on the level instrument.
U datin
Total
E ui ment Data
Base
TEDB
Ins ection Sco
e
37550
A review was
made by the inspectors of the licensee's
current efforts in
updating
and resolving problems with the TEDB.
Observations
and Findin s
The inspectors
reviewed the licensee's
current efforts and plans for
updating
and resolving problems with the TEDB.
The licensee
explained
the background for these efforts.
A review of Condition Reports
(CR)
was conducted in early 1997 to identify and assess
the generic concerns
related to this data
base
system.
The review identified 65 potentially
valid CRs which were further broken
down by causal
factors, e.g.,
calibration issues,
NRC/QA issues,
etc.
The predominant
issue
was
miscellaneous
setpoint/range
issues
for primarily non-safety-related
equipment.
The safety-related
setpoints
were determined to be
adequately 'controlled.
The seven
areas
were evaluated
using importance factors
and significance
factors
as multipliers.
The
NRC/QA issues
had the highest ranking with
TEDB procedure
revision/process
streamlining
second
and thi rd wa's the
setpoint/calibration
issues,
followed by the remaining four areas.
The
highest
concern involving regulatory/compliance
was given top priority
because it had the highest probability for impacting
a quality related
or safety-related
condition.
The potential existed for
misclassification for quality group or safety class.
Initial results
showed
numerous
upgrades
in classification were necessary.
The final
classifications
were determined to be accurate.
37
E2.3
E8
E8.1
E8.2
The CRs had recommendations
for corrective actions which, in a few
cases,
seemed to conflict.
The inspectors
discussed
the licensee's
new
system for streamlining the process for correcting
information in TEDB.
A new MEP,
No.
98012M, Revision 1, dated
March 19,
1998,
was
made
available for use in dispositioning various administrative,
non-safety-
related engineering
concerns.
A Change
Request
Notice
(CRN) would be
generated
against the generic
HEP and provide timely process for
addressing
certain
TEDB changes.
Setpoint
and calibration concerns.
as
they are found, would then result in prompt issuance of a
CRN to resolve,
the issues.
The licensee
was expending substantial effort each
month to
resolve the non-safety-related
problems with the TEDB system.
Conclusions
The licensee
has adequately controlled in a timely manner the safety-
related information in the TEDB.
The licensee's
new updating process
was adequate
and facilitated
a more timely resolution of non-safety-
related setpoints
and other design information issues
as they are found
in the TEDB.
The licensee
was allocating substantial
engineering effort
to resolve the problems with TEDB and to improve the support for the
18C
group maintenance
setpoint
and calibration program.
Nuclear Division En ineerin
Meetin
37551
On April 22, the inspectors
met with the Nuclear Division Engineering
staff in Juno
Beach to discuss current issues.
The Engineering staff
delivered presentations
on Turkey Point and St. Lucie Engineering
indicators, site self-assessments,
regulatory
and industry
issues'pecific
site problems
and their root cause
analyses,
and Engineering
initiatives.
The licensee
stressed
the fact that the Engineering
Division was unifying its approach to both sites..
The inspectors
found
the meeting informative.
Miscellaneous
Engineering
Issues
Closed
VIO 50-335 389/97-11-05
"Failure'o Maintain Motor 0 crated
Valve Calculations
Desi
n Documents
Su
ortin
Test Results
and
E ui ment Data
Base Current
and Consistent"
92903
The inspector
reviewed the licensee's
corrective
actions
as contained in
December
10,
1997.
Specific corrective
actions
reviewed are contained in paragraphs
El.l.b (1), (3), (6-'8),
and
(10) above.
The corrective actions
were acceptable.
This item 'is
closed.
Closed
URI 50-335 389/96-08-05
"Licensee Identified UFSAR
Deficiencies"
92903
The subject
URI was opened
as
a result of UFSAR reviews undertaken
by
the licensee to compare procedures
described in the
UFSAR with
operational
and other procedures.
At the time the URI was initiated,
the licensee
had identified 151 items for both units.
As the licensee's
38
review process is now complete,
the inspector
reviewed the results of
the process.
As a result of the licensee's
review effort. 1591
individual items were identified.
The inspector
reviewed six items, selected
at random.
from the
licensee's
database
of identified UFSAR accuracy issues.
All issues
were appropriately
documented,
entered into the licensee's
corrective
action process,
and were either resolved
or corrective actions were
specified
and completion dates
were established.
Of the sample
population, the inspector identified no violations.
Items reviewed
had
documented
cases
in which procedures
lacked
UFSAR references.
cases
in
which reviewers were, at the time of the review.
unaware of supplemental
information in the
UFSAR which provided context of the items identified,
= and cases
in which reviewers were unaware of procedures
which existed
which implemented
UFSAR commitments.
Of the items identified.
70 Unit 1
items'81 Unit 2 items,
and 42 procedural
revision items remained to be
resolved.
The project was scheduled to be completed in February of
1999.
The inspector concluded that the licensee
was appropriately
addressing
the items identified.
This item is closed.
Rl
Rl. 1
a.
IV. Pl ant Su
ort
Radiological Protection,and
Chemistry Controls
Review of Condition
Re ort=Re ardin
Containment Entries Without Health
~Ph
i
E
t
Ins ection Sco
e
71750
The inspector
reviewed the circumstances
surrounding Condition Report
(CR) 98-0340 which identified that personnel
entered the Unit 1
containment without a health physics
(HP) escort.
Observations
and Findin s
Condition Report 98-0340 stated that personnel
unescorted
by HP entered
a Locked High Radiation Area on February 22,
1998.
The inspector
reviewed the
CR and determined that the Locked High Radiation Area in
question
was the Unit 1 containment building.
At the time of the
incident the unit was shut
down to perform repai rs on
pump
(RCP) motor.
The
CR stated that the containment
was not actually
a Locked High
Radiation area,
but rather
had been "over posted."
An area inside the
containment
between the reactor coolant piping and the reactor
vessel
met the requirements
to be posted
as
However. signs
used to post radiological areas
were not allowed in that
area of containment
because
they could become dislodged, travel to the
containment
sump and block the strainers.
As
a result the licensee
moved the posting to the entrance of the containment.
~
~
39
F2
F2.1
Through interviews conducted,
the inspector determined that two
individuals had entered the containment to work on the
RCP motor without
HP escort.
One of the individuals was
a qualified
HP and the other was
with electrical
maintenance.
The inspector determined that the
maintenance
worker had been briefed by HPs prior to entering the
containment.
He was directed
as to the path to take after entering the
containment
and was told that
he would be met along the route by an
technician.
After the individual was briefed the
HP at the
RCP inside
the containment
was contacted
and told that
a worker would be entering
shortly.
The maintenance
worker stated that the path was well marked
and he was met by the
HP close to the
RCP.
The inspector
reviewed Procedure
HPP-3,
Revision 6, "High Radiation
Areas." regarding the requirements for entry into the'ontainment
or
a
Step 7.7.3 of that procedure stated that
"All entries into locked high radiation areas
require constant
coverage
by a qualified Health Physics technician with a dose rate instrument."
Appendix A, Step 9.A, stated that "Locked High Radiation Areas
and Very
High Radiation Areas requi re continuous
Health Physics
coverage."
Step
13.A defined continuous direct coverage
as,
"coverage
performed by a
qualified Health Physics individual who is in or near the area with
workers at all times and maintains
exposure control
on
a continuous
basis."
After discussing the circumstances
surrounding this event with
the
HP supervisor
and others involved'he inspector
concluded that
adequate
HP coverage
was provided to the maintenance
worker.
A review
of the radiation work permit for the
RCP motor repai r indicated that the
exposures
were below the prescribed limits.
The inspector noted that one of the corrective actions identified in the
CR was to procure posting materials that could be used in containment.
Conclusions
The inspector concluded that adequate
HP coverage
was provided for
individuals entering the Unit 1 containment to repai r a Reactor
Coolant
Pump.
Status of Fire Protection Facilities and Equipment
0 erabilit
of Fire Protection
Water
S stem and Fire
Pum s.
64704
Ins ection Sco
e
64704
In conjunction with the
NRC Fire Protection Functional
Inspection
(FPFI
Report
No. 50-335,
389/98-201)
conducted during the Narch 9.
1998,
and
April 3.
1998, time period, the inspectors
reviewed station
open
maintenance
work orders
and Condition Reports
(CRs),
issued for the
facility's fire protection water system
and fire pumps,
and performed
a
walkdown inspection of the equipment to assess
the material conditions
and performance trends.
40
Observations
and Findin s
Maintenance
Observations:
The review of station
open maintenance
work orders listed as of March
30.
1998. indicated that the total
number of open maintenance
work
orders related to the fire protection water system
and fire pumps
was
17.
. The inspectors
noted that very few (only 2) of the fire protection water
system
(System
15) work orders
(W/0) above were associated
with fire
protection water supply system piping or the fire pumps.
These
items
involved backfill for fire water piping (W/0 No. 980006075)
and repair
of a mounting discrepancy of the fire pump discharge
pressure
(W/0 No. 97012288).
These work orders
were minor repairs which did not
affect the operability of the fire protection water system or fire
pumps.
Work was properly scheduled to correct these
issues.
There was
not
a high backlog of open work orders for fire protection water system
or fire pumps.
Fire Protection Condition
Re orts:
The inspectors
evaluated
approximately
150 licensee fire protection
related
CRs initiated from January
1997 to March 30.
1998, that were
listed in the Condition Report Tracking database.
Most of the
identified issues
were the result of the licensee's
on-going Appendix
R
reassessment
effort.
Only five of the licensee
CRs initiated during
this period involved the fire protection water supply system piping or
the fire pumps.
The inspectors
concluded that the maintenance
and material condition of
the fire protection water
system
components
and fire pumps
was good.
The number of open Condition Report deficiencies identified as part of
the station problem evaluation process
associated
with the fire
rotection water system components
or the fire pumps
was small.
The
icensee's
corrective action dispostioned for resolution of fire
protection system problems
was being properly scheduled.
Conclusions
The maintenance
and material condition of the fire protection water
system
components
and fire pumps
was good.
There was not
a high backlog
of open work orders associated
with the fire protection water system
components
or the fire pumps.
The number of open Condition Report
deficiencies identified as part of the station problem evaluation
process
associated
with the fire protection water
system
components
or
the fire pumps
was small.
The licensee's
corrective action dispostioned
for resolution of fire protection system problems
was being properly
scheduled.
41
V. Mana ement Meetin s and Other
Areas
X1
Exit Meeting Summary
The .inspectors
presented
the inspection results to members of licensee
management
at the conclusion of the inspection
on May 14. '1998.
Interim
exit meetings
were held on April 3 and April 9,
1998 to discuss
the
findings of Region based inspection.
The licensee
acknowledged
the
findings presented.
The inspectors
asked the licensee
whether
any materials
examined during
the inspection should
be considered proprietary.
No proprietary
information was identified.
Licensee
PARTIAL LIST OF
PERSONS
CONTACTED
M. Allen. Training Manager
C. Bible, Site Engineering
Manager
W. Bladow, Site Quality Manager
D. Fadden,
Services
Manager
R. Heroux, Business
Manager
'.
Johnson,
Operations
Manager
J.
Marchese.
Maintenance
Manager
C. Marple, Operations
Supervisor
R. McDaniel, Fire Protection Supervisor
J. Scarola.
St. Lucie Plant General
Manager
A. Stall. St. Lucie Plant Vice President
E.
Weinkam, Licensing Manager
Other licensee
employees
contacted
included office, operations,
engineering,
maintenance,
chemistry/radiation,
and corporate personnel.
INSPECTION
PROCEDURES
USED
IP 37550:
Engineering
IP 37551:
Onsite Engineering
IP 61726:
Survei'llance Observations
IP 62707:
Maintenance
Observations
IP 64704:
Fire Protection
IP 71707:
Plant Operations
IP 71750:
Plant Support Activities
IP 92901:
Followup - Plant Operations
IP 92902:
Followup
-- Maintenance
IP 92903:
Followup - Engineering
TI 2515-109:
Inspection
Requirements
for GL 89-10
~
~
~0ened
42
ITEMS OPENED
CLOSED
AND DISCUSSED
50-335 '89/98-06-01
"Repeat Failure to Implement
an Equipment
Clearance
Order Prior to Beginning Work"
(Section 01.2)
50-335.389/98-06-02
. "Failure to Fulfill a Technical Specification
Surveillance
Requirement to Continuously Monitor
Oxygen Concentration in the Gas
Decay Tank"
(Section 02.1)
50-335,389/98-06-03
50-335.389/98-06-04
Closed
50-389/97-05-01
50-335,389/97-11-05
50-335,389/96-08-05
Discussed
50-335/97-01-01
50-335/97-03-01
50-389/97-04-01
50-335/97-06-01
IFI
VIO
"Corrective Action Program Lacks Focus
on
Correction of Problems" '(Section 07.6)
"Completion of Motor Operated
Valve Program
Follow-up Items" (Sections
El. 1)
Failure To Control Foreign Material Entering
and Exiting the Unit 2 Containment"
(Section
HB. 1)
"Failure to Maintain Motor Operated
Valve
Calculations,
Design Documents,
Supporting Test
Results,
and Equipment
Data
Base Current
and
Consistent"
(Section
E8. 1)
"Licensee Identi fied UFSAR Deficiencies"
(Section E8.2)
"Failure to Follow In-Plant Equipment Clearance
Order Procedure"
(Section 01.2)
"Failure to Adequately
Implement
an Equipment
Clearance
Order" (Section 01.2)
"Failure to Follow The Equipment Clearance
Order
Procedure"
(Section 01.2)
"Failure to Implement
an
ECO Prior to Beginning
Work" (Section 01.2)
50-335/97-14-03
<"Failure to Proper ly Execute
an Equipment
Clearance
Order" (Section 01.2)
0
~
~~
ADM
ANPS
ATTN
CFR
CNRB
CR
CRN
ECO
ENG
FRG
GDT
GL
GMP
HPP
i.e.
e.g.
I8C
IFI
INEEL
IP
IR
JCN
JPE
JPN
LER
LHR
MEP
NaOH
NRC
NWE
43
LIST OF ACRONYMS USED
Administrative Procedure
(system)
As Low as Reasonably
Achievable (radiation
Assistant
Nuclear Plant Supervisor
Administrative Procedure
Attention
Corrective Action Plan
Control
Element Assembly
Code of Federal
Regulations
Company Nuclear Review Board
Condition Report
Change
Request
Notice
Equipment Clearance
Order
Engineering
Electric Power Research
Institute
Engineered
Safety Feature Actuation System
The Florida
Power
8 Light Company
Facility Review Group
Final Safety Analysis Report
Gas
Decay Tank
[NRCj Generic Letter
General
Maintenance
Procedure
Health Physics
Health Physics
Procedure
that is
for example
Instrumentation
and Control
[NRCj Inspector Followup Item
Idaho National Engineering
and Environment
Inspection
Procedure
[NRC] Inspection Report
Juno Change Notice
Joint Owners Group
(Juno Beach)
Power Plant Engineering
Job Performance
Measurement
(Juno Beach) Nuclear Engineering
Licensee
Event Report
Locked High Radiation
Motor Operated
Valve
Minor Engineering
Package
Sodium Hydroxide
Non-Cited Violation (of NRC requirements)
Non-licensed
Operator
Nuclear Plant Supervisor
Nuclear Regulatory Commission
Nuclear Regulatory
(NRC Headquarters
Publi
Nuclear Watch Engineer
exposure)
al Laboratory
cation)
~
~y
0
03F
PMAI
psld
PSL
QI
RCO
TEDB
.
TS
Operating
Experience
Feedback
On-the Job Training
NRC Public Document
Room.
Plant Managers Action Item
Power Operated Relief Valve
Performance
Prediction Methodology
Pounds
per square
inch (differential)
Plant St. Lucie
Quality Assuran'ce
Quality Instruction
Quality Surveillance Letter
Reactor Auxiliary Building
Reactor Control Operator
Pump
Reactor
Coolant System
Reactor
Protection
System
Systems
and Component
Engineering
Significant Condition Report
Saint
Tempora'ry
Change
Total
Equipment
Data
Base
Technical Specification
Updated Final Safety Analysis Report
[NRC1 Unresolved
Item
United States
Nuclear Regulatory
Commission
Violation (ot
NRC requirements)
Vice President
Work Control Center
Work Order