ML17229A560
| ML17229A560 | |
| Person / Time | |
|---|---|
| Site: | Saint Lucie |
| Issue date: | 12/18/1997 |
| From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML17229A558 | List: |
| References | |
| 50-335-97-13, 50-389-97-13, NUDOCS 9712300093 | |
| Download: ML17229A560 (59) | |
See also: IR 05000335/1997013
Text
U.S.
NUCLEAR REGULATORY COMMISSION
REGION II
Docket Nos: 50-335.
50-389
License
Nos:
Report
Nos: 50-335/97-13,
50-389/97-13
Licensee:
Florida Power
& Light Co.
Facility:
St. Lucie Nuclear Plant.
Units
1
& 2
Location:
6351 South
Ocean Drive
Jensen
Beach,
FL
34957
Dates:
October
12 - November 22,
1997
Inspectors:
J.
Hunday, Senior
Resident
Inspector,
Acting
D. Lanyi, Resident
Inspector
J.
Blake,
Regional
Inspector
(Sections Hl.6, Hl.7,
H1.8, M3.1, H5.1,
and H7.1)
F. Wright. Regional
Inspector
(Sections Rl.l, R1.2,
R1.3,
R2.1,
and R5.1)
P.
Harmon,
Licensing Inspector
(Section 05.1)
S. Rudisail.
Regional
Project Engineer
(Sections 08.3,
E8.2,
E8.3,
and E8.4)
R. Chou,
Regional
Inspector
(Sections
E1.1,
E1.2,
and
E1.3)
L. Stratton,
Regional
Inspector
(Sections
S1.3,
S5.1.
S8. 1,
and S8.2)
J. Williams,
NRR Project
Manager
(Sections
08.2. Ml.9.
and E8.1)
Approved by:
K. Landis, Chief. Reactor Projects
Branch
3
Division ot Reactor
Projects
Enclosure
2
9712300093
97i2%8
ADQCK 05000335
8
EXECUTIVE SUMMARY
St. Lucie Nuclear Plant, Units
1
8
2
NRC Inspection Report 50-335/97-13,
50-389/97-13
This integrated
inspection included aspects
of licensee
operations,
engineer-
ing, maintenance,
and plant support.
The report covers
a 6-week period of
resident inspection;
in addition, it includes inspection in the areas of steam
generator
replacement activities, radiological protection,
licensed operator
requalification,
and security.
0 erations
~
The licensee
performance
during the Unit 1 shutdown
was professional
and
in accordance
with site procedures.
The inspector
noted two minor
problems
caused
by inadequate
planning,
but Operations
successfully
worked through these
problems.
(Section 01.1)
~
The licensee
obtained
a primary coolant sample successfully in
accordance
with the appropriate
procedure.
The Chemistry Technician
was
knowledgeable
about the evolution.
(Section 04. 1)
The inspector
concluded that requalification activities were adequately
implemented during the inspection
week but several
weaknesses
were
observed in both training programs
and operator
performance.
(Section
05.1)
The inspector
concluded that the licensee's
response to a lodged
CEA was
extremely well planned
and coordinated.
Examples of excellent
communication
and team work were noted.
(Section 08. 1)
The inspectors
concluded the core offload was completed safely and with
an adequate
amount of licensee oversight.
Additionally. the inspector
noted that activities associated
with a misgrappled fuel bundle were
completed in a deliberate
and safety-conscious
manner.
(Section 08.2)
Maintenance
Nine maintenance activities were observed
and noted to have generally
been completed thoroughly and professionally.
Good
FHE control
and
procedural
adherence
was also observed.
(Section Ml.5)
Replacement
Project equipment
removal
and welding
activities were being conducted in accordance
with approved
plans
and
procedures.
(Section Ml.6)
The licensee
continued to maintain
a well-organized
program for
monitoring flow accelerated
corrosion.
(Section H1.7)
The scope of the In Service Inspection
and planned preservice
inspections
were appropriate.
(Section M1.8)
Enclosure
2
The inspector concluded that the transfer of Incore Instrument
remnants
from the Unit 1 reactor vessel to the spent fuel pool was carefully and
thoroughly planned
and completed with low radiation dose
expended.
(Section M1.9)
Welding procedures
for the Steam Generator
Replacement
Project were
complete
and appropriately qualified in accordance with required welding
standards.
(Section M3.1)
Replacement
Project welder training and qualification
activities were being conducted in full compliance with ASME Section
IX
requirements.
(Section
M5. 1)
The licensee's
Nuclear Assur ance surveillance activities provided
a
comprehensive
review of'he contractor 's welding and welding inspection
activities.
(Section
M7. 1)
En ineerin
The inspectors
concluded that the preparation of engineering
and heavy
load lifting of the original and replacement
was
acceptable
per the design
drawings
and was adequate
to provide the
stabilization of the steam generators
for removal.
(Sections
El. 1,
E1.2)
One violation was identified for the absence
of travel limit markings
on
the steam generator
temporary lifting device.
(Sections
E1.3)
~
Overall. the removal of the original steam generators
and the
installation of the replacement
was completed without
incident.
(Section
E1.3)
~
The full core offload safety evaluation
was well presented
and clearly
documented
the lack of any unreviewed safety questions.
The evaluation
was properly translated into the applicable procedures
to ensure that
the evaluation
was valid.
(Section
E2. 1)
Plant
Su
ort
The Health Physics Project Overview documents
developed to instruct and
establish
radiological controls for unique Steam Generator
Replacement
Project
(SGRP) tasks
were an excellent planning resource.
(Section Rl. 1)
The inspectors
confirmed that As Low As Reasonably
Achievable
and
Radiation Protection concerns
were factored into the
SGRP planning.
Section Rl. 1)
With the exception of the pressurizer
heater
replacement
project, the
licensee
was effectively estimating
and tracking collective doses
for
Enclosure
2
planned tasks.
(Section R1.1)
Collective dose for the pressurizer
heater project was significantly
underestimated.
(Section Rl. 1)
Good radiation protection control measures
were in place inside the
licensee's
Radiation Control Area and overall licensee
exposure controls
were effective.
(Section R1.1)
Good use of remote radiation monitoring technology to monitor work in
radiation
and high radiation areas to save collective dose
was observed.
(Section R1.1)
Licensee contamination controls were effective.
(Section Rl. 1)
Licensee radiation protection controls for the construction
hatch were
appropriate
and effective.
(Section
R1. 1)
Inadequate
radiation worker awareness
of Radiation
Work Permit
(RWP)
requi rements
were identified as violations of the licensee's
radiation
protection procedures
and licensee's
Technical Specifications
(TSs).
(Section R1.2)
Inadequate written procedures
for the issuance of tele-dosimetry
and
setting dosimeter
setpoints
in agreement with the
RWP requi rements
was
identified as violation of licensee's
TSs.
(Section R1.2)
A Non Cited Violation was identified for failure to follow procedures
for securing
access to a Very High Radiation Area.
(Section R1.3)
The licensee
established
excellent Radiation Protection support
facilities for the
SGRP.
(Section
2. 1)
The licensee established
good Radiation Protection controls for the
removal
and movement of the Original Steam Generators
to the Interim
Storage Facility.
The licensee
was well prepared to temporarily store
and ship the Steam Generators
to a disposal facility.
(Section
R2. 1)
Radiation Protection staffing levels were sufficient to provide good
radiation protection support for the planned outage activities.
(Section R5.1)
Training activities for radiation workers
and Health Physics Technicians
concerning
Steam Generation
Replacement
Project activities were
appropriate.
(Section
R5. 1)
The inspector concluded that the licensee's
fitness for duty program was
being implemented in accordance
with 10 CFR 26.
(Section S1.3)
The protected
area barriers were in good condition, the isolation zones
Enclosure
2
i
well lit, and the appropriate
compensatory
guard postings in place.
(Section
S2. 1)
~
The licensee's
planned
compensatory
measures,
removal of vital area
barriers.
and access
control of containment during the steam generator
replacement
project were appropriate
and met the requirements
specified
in the Plant Security Plan.
(Section
S8. 1)
Enclosure
2
Re ort Details
Summar
of Plant Status
Unit
1 operated
at essentially full power until October 20,
when the licensee
shut
down the unit for the Steam Generator
Replacement
Outage.
The plant
remained shut
down for the remainder of the report period.
Unit 2 operated at essentially full power throughout the entire report period.
IIOI ti
01
01.1
01.1
Conduct of Operations
General
Comments
71707
Using Inspection
Procedure
71707, the inspectors
conducted
frequent
reviews of'ngoing plant operations.
In general.
the conduct of opera-
tions was professional
and safety-conscious;
specific events
and
noteworthy observations
are detailed
in the sections
below.
Unit 1 Shutdown for Steam Generator
Re lacement
Outa
e
71707
Inspection
Scope
At approximately
12:10
am on October
20, the licensee
removed Unit
1
from the grid in preparation for the Steam Generator
(SG) replacement
and refueling outage.
The inspector
observed the pre-evolution
briefings, turbine shutdown,
reactor
shutdown
and Hain Steam Isolation
Valve (HSIV) stroking.
Observations
and Findings
On the evening of October
19, the licensee started the Unit 1 shutdown
in preparation f'r the
SG replacement
outage.
The Assistant
Nuclear
Plant Supervisor
(ANPS) conducted
a detailed briefing for the evolution
shortly after 7:00
pm.
The brief was attended
by all affected
Operations
personnel,
Reactor
Engineering,
Chemistry,
and Hanagement.
Overall. the inspector
found the brief to be well organized
and
generally informative.
The inspector
noted that the crew'
participation was good and noted the crew made several
excellent
suggestions
to help the shutdown
go more smoothly.
At approximately 8:00
pm, Operations
began lowering turbine load in
accordance
with Procedure
NOP-1-0030125,
Revision 4, "Turbine Shutdown-
Full Load to Zero Load."
The operators
handled the down power
conscientiously
and professionally.
The inspector
noted good
coordination
between the operators,
their supervision,
and Reactor
Engineering.
The ANPS and Nuclear
Plant Supervisor
(NPS) maintained the
extraneous activity level in the control
room to a minimum.
The output
breakers for the main generator
were opened at 12: 10
am on October 20.
Enclosure
2
02
02.1
Operations
maintained the unit around
8 percent reactor
power for a half
hour to perform Steam
Bypass Control System
(SBCS) testing.
This test
assured
the licensee that the
SBCS would operate
as required to allow a
rrormal cooldown of the plant.
The system worked as expected.
After
completion of the test,
the operators
commenced
a reactor
shutdown
and
cooldown in accordance
with Procedures
NOP-1-0030128,
Revision 0,
"Reactor Shutdown,"
and NOP-1-0030127,
Revision 7, "Reactor Plant
Cooldown
- Hot Standby to Cold Shutdown."
The plant entered
Hode
2 at
12:48
am and
Hode 3 at 1: 15 am.
One issue in particular presented
a minor problem to the Operations
crew.
Several
months
ago, the licensee
adjusted the packing
on the
1A
HSIV.
This required the valve to be fully stroked
and timed as
a
retest.
This was not preplanned for the night and the Operating
crew
had to adjust thei r plan for the shift.
The inspector
observed
several
discussions
between the ANPS, the
NPS, the Nuclear
Watch Engineer
(NWE),
the Shift Technical Advisor (STA), and the board operators
about the
subject.
They determined
an appropriate
course of action that
procedures
encompassed.
The inspector then observed the
ANPS hold
"mini-briefs" with one or two individuals to discuss this plan.
At that
point, the inspector
believed that
a full crew brief would have
been
more efficient and beneficial.
About one half hour after disseminating
the plan, the
ANPS did perform
a satisfactory full crew brief.
The inspector
noted only one other
minor delay.
The licensee
knew about
two Control
Element Assemblies
(CEAs) in particular that had been
known
to drop when moved.
The licensee
had resolved this problem in the past
by installing temporary control cards.
As the operator
approached
the
first group with one of these
CEAs, Operations
had difficulty contacting
18C to get the card installed.
CEA insertion
was delayed approximately
25 minutes while waiting for the card to be installed.
The shutdown
continued without further incident.
The secondary
system
was aligned
for the A HSIV test shortly after 4:00
am and the valve was stroked
satisfactorily.
Conclusions
The licensee
performance during the Unit 1 shutdown
was professional
and
in accordance
with site procedures.
The inspector noted two minor
problems
caused
by inadequate
planning, but Operations
successfully
worked through them.
Operational
Status of Facilities and Equipment
En ineered Safet
Feature
S stem Walkdowns
71707
The inspectors
used Inspection
Procedure
71707 to walk down accessible
portions of the following Engineered
Safety Feature
systems within the
Unit 1 containment:
Enclosure
2
04
04.1
05
~
Safety Injection Tanks
~
Low Pressure
Safety Injection System
~
High Pressure
Safety Injection System
Equipment operability, material condition,
and housekeeping
were
acceptable
in all cases:
Several
minor discrepancies
were brought to
the licensee's
attention
and were corrected.
The inspectors identified
no substantive
concerns
as
a result of'hese
walkdowns.
Operator
Knowledge and Performance
Unit
1 Primar
Sam le Observation
71707
Inspection
Scope
On October
17, the inspector
observed
a Chemistry Technician
draw and
analyze
a primary sample
on Unit 1.
The inspector verified procedural
compliance,
confirmed good laboratory technique,
and surveyed the
technician's
general
knowledge.
Observations
and Findings
The inspector
observed
a Chemistry Technician
draw
a Unit
1 primary
sample in accordance
with Procedure
1-COP-65.21,
Revision 4, "Unit 1
Primary Systems
Sampling."
The inspector
noted that the technician
was
thoroughly familiar with the sampling procedure.
A current revision of
the procedure
was available at the sample sink,
and the technician
routinely referred to it throughout the sampling process.
The inspector
was satisfied that the sample
was drawn properly.
The inspector
then observed
the technician perform the analysis of the
sample.
The inspector
asked several
questions relating to the use of
the analytical
equipment,
the timing of samples,
and the expected
results.
All questions
were answered
by the technician to the
inspectors satisf'action.
The inspector
noted that the technician's
laboratory technique
was very good, minimizing any potential f'r
inadvertently contaminating
equipment
and ensuring that the sample did
not become accidentally adulterated.
The inspector verified that all results
observed
were within the
prescribed
Technical Specification limits.
No discrepancies
were noted.
Conclusions
The inspector
concluded that the primary sample
was performed in
accordance
with procedures,
and the Chemistry Technician
was
knowledgeable
about the evolution.
Operator Training and Qualification
Enclosure
2
05.1
a.
4
Licensed
0 erator
Re uglification Pro ram
71001
Inspection
Scope
The
NRC conducted
a routine.
announced
inspection of the licensed
operator Requalification program during the period of November 17-21,
1997.
The inspector
reviewed
and observed
annual Requalification
examinations
conducted
by the licensee
and conducted
inspection
activities to determine
compliance with 10 CFR 55.59, "Requalification,"
using Inspection
Procedure
71001.
Activities reviewed included
examination
development
and administration,
evaluator performance,
simulator scenario
and Job Performance
Measure
(JPMs) evaluations.
Observations
and Findings
Written Examination
The inspectors
reviewed the sample plan developed for the examination
which covered the last two year cycle.
The overall sample plan
construction
adequately
covered the material
presented for the
Requalification cycle.
The examinations
were developed with the intent
to prevent overlap between the diff'erent sections of the annual
examination.
This prevented
excessive topic or subject overlap.
The inspector
reviewed the Senior
Reactor Operator
(SRO) written weekly
quizzes administered
November
13,
and
November
14,
1997.
The quizzes
were administered
as
"open reference"
type exams, with references
limited to Control
Room material.
The "A" quiz was administered to 10
operators.
and the "B" quiz to 13 operators.
The quizzes
covered the
same week's instructional material,
and consisted of 20 questions
each'f
which 10 questions
were
common to both tests.
The inspector
discussed
several
questions with the exam author concerning question
stem development,
distractor
improvement,
and level of difficulty.
Approximately half the questions
on each quiz would have required
some
changes to be fully acceptable.
Most of the changes
involved making one
or more of the distractors credible.
The questions,
in most instances,
requi red an appropriate
amount of analysis
and synthesis of the provided
information to correctly answer
the questions.
However, the extremely
high scores
indicate the overall discrimination level of the quizzes
may
have been too low.
The results also indicate that individual questions
may have been too simplistic or contained construction deficiencies
which allowed
a high rate of correct answers.
The licensee's
exam
administration policies requi re an evaluation of questions
having
a 40
percent or more error rate.
but does not require evaluating questions
with a
100 percent correct
answer rate.
This tends to bias
an exam bank
toward the more "successful"
questions.
However, the 100 percent
questions
do not provide meaningful
feedback to the program.
In effect,
there is no discrimination value for a question which is answered
correctly 100 percent of the time.
The sample size of 10 and
13
students
is too small to provide an absolute determination of
Enclosure
2
5
discrimination level based
on success
rates,
but questions
receiving
100
percent correct answers
should
be evaluated
as aggressively
as questions
receiving too low a correct
answer
rate.
The "A" quiz results
were: All 10 students
answered
14 of 20
questions correctly.
9 of 10 students
received
scores of 90
percent
or greater,
lowest score
was
85 percent.
The "B" quiz results were:
All 13 students
answered
10 of 20
questions correctly.
'12 of 13 students
receive scores of 90
percent or greater,
lowest score
was
85 percent.
The written exam deficiencies
are similar to those previously identified
during an
NRC inspection of the licensee's
Requalification program and
detailed in Inspection
Report 50-335,389/96-20.
Simulator Scenario Construction
The inspector
reviewed the dynamic simulator scenarios
administered
during the inspection
week.
The inspector also witnessed
two scenarios
presented
to
a single crew.
The dynamic scenarios
were considered
appropriately challenging
and were an excellent
assessment
tool.
The
scenarios
provided opportunities to evaluate the competency of operators
in all pertinent areas.
Simulator
and In-Plant Job Performance
Measures
Evaluators effectively queried the operators
using follow-up questions
based
upon operator
performance.
This allowed the evaluators to
determine generic or individual areas
needing
improvement.
There were
no JPM failures observed.
JPMs were considered to be of very good quality and were appropriately
discriminating.
A less-than-qualified
individual would not be expected
to successfully
complete the JPMs.
This evaluation
area
should provide
good feedback to the Requalification Training program.
0 erator/Evaluator
Performance
The inspector
observed
a single crew's performance
during two simulator
scenarios.
The inspector's
evaluation of the crew's performance
differed significantly from that of the licensee.
The crew being
evaluated tripped the reactor
unnecessarily
based
on
a single failed
indicator, erroneously
declared
a Site Area Emergency
(which resulted in
an unnecessary
Site Evacuation).
and failed to consider the effects of a
faulted emergency
power supply on safeguards
equipment.
In addition,
the crew neglected to attend
numerous
alarms
and annunciators.
Despite
these errors,
the evaluators
passed
the crew overall without
remediation.
The crew was
a staff crew that had not had experience
working together.
However, their overall performance
was not considered
Enclosure
2
satisfactory
by the inspector.
The inspector
attended
the evaluators'valuation
and debriefing of the
crew.
The evaluators correctly identified the technical errors
by the
crew, but appeared tolerant of the mistakes.
In fact.
one evaluator
offered explanations
and excuses f'r some of the errors to the
inspector.
The inspector
concluded that the evaluators
used
good
techniques
and were observant of most of the crew'. errors,
but were not
sufficiently aggressive
and demanding in their conclusions.
The errors
would have resulted in a crew failure during an NRC-administered
examination.
As
a minimum, several
areas of remediation should
have
been stipulated
by the evaluators.
This appears to be an instance of
negative training or feedback to the individual crew members.
0 erator
Performance
During the simulator scenarios,
operators
on numerous
occasions
did not
respond to alarms,
missed
some alarms completely,
and were not
conscientious
in attending,
acknowledging,
or responding to alarms.
The
inspector
noted
a single exception to the general
lack of response
to
alarms.
A back, auxiliary alarm panel
always received
prompt attention
from the operators.
This particular
panel
was not unique in the safety
significance of the items monitored.
but instead
had
an audible alarm
that was irritating in nature
and did not time out in three seconds.
The inspector
concluded that the present
design of the audible portion
of the general
alarm system is conducive to inappropriate
operator
response to those alarms.
The facility appears to be
an outlier in
regards to audible alarms timing out within three seconds.
This issue
was discussed
in detail with licensee
management.
During the
inspection,
licensee
management
agreed to evaluate the alarm system
design.
During simulator
JPMs,
operators
frequently placed
books
and procedure
manuals
on the control panel.
In one instance.
an operator
propped
an
open book against the rod position (in-hold-out) switch when he moved
away from the panel.
The book was
a light, Accopress
binder
which
probably would not have
been
heavy enough to move the rod control
switch.
The inspector
noted that there are no provisions for operators
to put their books
and manuals
down for easy reference
other than the
control board or a relatively inaccessible
table or desk behind them.
This makes attending the control board while referring to procedures
extremely difficult.
As
a consequence,
operators
have introduced
an
unintended work-around in the manner in which they place reference
material
on the control board.
When questioned
about why they tolerated
such
a poor design.
several
operators
said that past requests
to have
a
shelf placed
on the panel
were not accepted.
The operators
were not
able to provide any information on formal requests.
corrective action
initiatives, or any other corroborating evidence that the issue
was
aggressively
pursued.
The inspector
concluded that operators
have
been
aware of an unacceptable
condition,
made limited efforts to effect
a
Enclosure
2
change,
but eventually accepted
the condition without taking
a strong
stand.
During performance of JPM 0821082,
Realigning
a CEA, three of four
operators
interpreted
a procedural
caution to "maintain reactor
power
constant"
during the
CEA realignment
as requiring boron changes
during
the rod movement.
The realignment involved minor reactivity changes
from the
CEA (12 inches total travel,
rods near the,top of the core),
and could have been accomplished relatively easily without boration.
Because of thei r sensitivity to maintaining reactor
power constant,
those operators
who elected to change
boron concentrations
took much
longer to restore the
CEA and in fact caused
more power changes
because
of the lagging effect of boron changes
on reactor
power (over- and
under-shoot).
Since the recovery procedure is not prescriptive in the
methodology of holding power constant or in what constant
means,
one
operator simply pulled the
CEA and accepted
the relative minor reactor
power
change.
All operators
were evaluated
as "satisfactory" in how
they performed this JPM.
The inspector concluded that the procedure
should
be reviewed for enhancement,
especially in defining whether
"constant" should
be defined
as
some acceptable
range.
The procedure
could also provide guidance
on
a rough calculation of the total
reactivity associated
with a realignment
and better guidance
on whether
the total change
should
be accompanied
by
a boration change.
The
inspector also noted that the operator
was required to make
a total of
four phone calls to operations
management
and to Reactor
Engineering
prior to and after the
CEA realignment.
If this procedure is considered
critical enough for this level of'pproval or notification, direct
assistance
from those contacted
may be indicated.
Otherwise,
simply
making notification provides
no real support to the operators.
In addition to the boron changes
described
above,
the lack of
consistency
on defining "constant" also caused
operators to consult
additional
power level indicators while making reactivity changes
for
the
CEA Realignment
JPM.
A digital readout indicator
on the safeguards
panel behind the operators
was frequently checked while making boron
changes
and manipulating rods.
This required all four operators to turn
around to view this instrumentation.
The inspector
asked the operators
after the
JPM performance
why they were watching the back panel
indicators rather
than the power level indicators directly in front of
them at the rod control panel.
The operators
indicated that the back
anel indicators were "real-time" while the rod control panel indicators
ad
a considerable
lag time due to computer updating.
and that the
digital readouts
on the back panel
were superior in their display of
reactor
power to two decimal
places.
Therefore,
they were better for
complying with the requi rement to hold power "constant."
The inspector
considers this condition to constitute
a work-around.
Either the
indicators
on the rod control panel
are perfectly acceptable for such
reactivity maneuvers
or appropriate indicators should
be provided at the
panel.
If operators
are misinterpreting the requirement to keep power
constant,
appropriate training should
be provided.
The inspector
Enclosure
2
08
08.1
informed the licensee that this issue should
be evaluated
and resolved.
Turning away from the control panel
during reactivity manipulations
should only occur when absolutely required,
not as routinely as observed
during this JPM.
Operators
did not use the Alarm Response
Procedures
(ARPs) in a
consistent
manner.
The ARPs in use
on the simulator are very sketchy
and provide minimal information to the operators.
When questioned,
both
evaluators
and staff told the inspector that one unit has already
upgraded the ARPs,
and. the other unit's
ARPs are being upgraded.
Pro
ram Feedback
The inspector
reviewed records
and followup documentation of student
and
management
observation
feedback to the Requalification
Program.
The
training staff treated
feedback in a thoroughly professional
manner.
Feedback
was afforded the right level of respect
and skepticism where
warranted.
Suggestions
and complaints were handled
and pursued in an
appropriate
manner.
Conclusions
The Requalification program met all regulatory standards
and
requi rements
during this training cycle.
The written weekly quizzes
were considered
minimally discriminating and provided little effective
feedback to the program.
Simulator
scenarios
and
JPMs were
appropriately discriminating
and were well organized.
Operators
were
knowledgeable of the plant and systems,
but did not display good
corroboration
and verification techniques.
Operators
were frequently
inattentive to the control panels
and alarms.
Evaluators did not
aggressively
implement management
standards
in the area of'onduct of
Operations.
Evaluators
were tolerant of both minor mistakes
and major
errors. to the point of providing negative
feedback
on thei r
acceptability.
Operators
were tolerant of unacceptable
conditions,
and
were not aggressive
in ensuring their resolution.
Procedural
weaknesses,
control
room human factor deficiencies,
and work-arounds
were not identified and aggressively
pursued
by operators
or evaluators.
Miscellaneous
Operations
Issues
Control Element Assembl
Lifted Durin
U
er
Guide Structure
Removal
71707
93702
Inspection
Scope
Whi'le lifting the upper guide structure
(UGS), from the Unit I reactor
pressure
vessel
(RPV), the licensee
noted
a Control Element Assembly
(CEA). lodged in the
UGS and fully withdrawn from the core.
The
inspector monitored the activities associated
with the retrieval of the
CEA as well as the procedure
changes
and evaluations that were necessary
Enclosure
2
to accomplish the task.
b.
Observations
and Findings
On October 27. the licensee lifted the
UGS in preparation for defuelling
the reactor.
Once lifted, an underwater
inspection of the bottom side
of the
UGS was performed, to determine if there were any interferences
with other
reactor internal
components.
During the. inspection,
the
licensee identified a single
CEA protruding from the lower end of the
UGS.
The
CEA had apparently
lodged in the
UGS and was lifted from the
reactor core.
Upon identification, the licensee
immediately halted
further
UGS movement.
At the time of the event.
the containment
equipment
and personnel
hatches
were open to facilitate access
in preparation for replacing the
The licensee
subsequently
secured
those penetrations
and reestablished
containment integrity.
The licensee
revised the reactor disassembly
procedure
being used at the
time, General
Maintenance
Procedure
No 1-M-0015, Revision 36,
"Reactor
Vessel
Maintenance
- Sequence of Operations," to account for the
additional height the
UGS would have to be lifted for the
CEA to clear
the
RPV wall.
In addition, cautions
were added to account for the
expected
increase
in dose rates
as the
UGS was raised.
Shielding was
provided for the crane operator
as well as others
necessary
to complete
the task.
As the
UGS was moved,
a containment isolation occurred,
as expected,
due
to the increased
radi ation levels.
The
UGS was successfully
moved to
the equipment storage
area adjacent to the
RPV.
The entire
move was
videotaped with the aid of a submersible
"submarine"
camera.
However.
during the move, the tether attached to the submersible
became entangled
in the rodlets of the CEA.
The licensee
used the tether to free the
f'rom the
UGS and it fell, approximately
one foot, to the floor of the
storage
area.
The
CEA was then
moved to the fuel handling building for
inspection.
A high level of management
attention
was afforded this activity.
Hours
of work were reviewed to ensure that the job would be completed
by
personnel
that were rested
and alert.
Continuous inspection of the
activity via the submersible
proved to be
a tremendous
aid to ensure the
move route for the
UGS was acceptable.
The inspector attended
the Facility Review Group meeting which approved
the revision to the reactor disassembly
procedure,
and noted that the
review was methodical
and well thought out.
Contingencies
were
discussed
and preparations
made as
a result.
In addition, the inspector
witnessed the
UGS move.
The job was very well controlled,
both from an
ALARA perspective
as well as from a heavy lift perspective.
The total
dose received during the move was below 200
mR with the highest single
Enclosure
2
dose being 42 mR.
10
The inspector
reviewed the procedure the licensee
used while unlatching
the CEA's,
OP 1-0110022,
Revision 20. "Coupling and Uncoupling of CEA
Extension Shafts",
and concluded that it appeared
adequate
to properly
unlatch the CEAs.
Video tape of the
CEA and the extension shafts
were
reviewed but no conclusions
could be drawn
as to the ultimate cause of
the
CEA becoming
lodged.
Although the investigation into the root cause
of this event
was not complete,
the licensee
does plan to replace
both
the
CEA and the
CEA extension shaft prior to restart.
Conclusions
The inspector concluded that the licensee's
response to the lodged
was extremely well planned
and coordinated.
Examples of excellent
communication
and team work were observed
during the
UGS move,
as
evidenced
by the low dose received
by the personnel
performing the work.
His ra
led Fuel
Assembl
Durin
Unit 1 Core Offload
71707
Inspection
Scope
The inspectors
witnessed portions of the Unit
1 core offload during this
report period.
In addition, the inspector witnessed activities
associated
with a misgrappled fuel assembly.
Observations
and Findings
The inspectors
witnessed the licensee
remove fuel from the reactor
and
transfer it to the spent fuel pool, at various times during the offload.
The actual fuel movement
was performed by contractors with oversight
provided by the licensee.
The inspectors
observed the amount of
oversight provided to be adequate.
At 4:00
pm,
on October 29,
a refueling machine
over load condition was
observed
when the licensee
was attempting to remove fuel assembly
R33
from core location E-5.
Visual inspection of'he assembly
using
a
remote
camera
revealed that the refueling machine
had grappled
a fuel
assembly corner
post instead of the center post.
This misgrappling
misaligned the assembly,
such that it could not be withdrawn into the
hoist box,
and resulted in the overload condition when the assembly
was
attempted to be raised.
Appendix J of licensee
Pre-Operational
Procedure
3200090,
Revision 26,
"Refueling Operation" provided guidance
on diagnosing
and resolving
overload problems.
For unanticipated
circumstances.
this procedure
provided considerable
latitude to the Refueling Supervisor for
development
and execution of corrective actions.
Licensee
personnel
outlined
a sequence
of actions to return the misgrappled
assembly to its
original core location,
release
the grapple,
and then to regrapple over
Enclosure
2
the center post.
11
After briefing personnel
on the planned
sequence
of events.
the
refueling machine
was manually moved to coordinates
calculated to be
close to the assembly's
original location.
The licensee
used the video
camera to monitor the movement of the assembly
and verify that the lower
end fitting was properly aligned with the core support plate alignment
pins.
The assembly
was then lowered manually,
and the grapple released
at 8:55
pm, October 29.
The assembly
was observed to be bowed
approximately
3 inches east;
and 0.5 inches north.
The video camera
was
used to monitor the grapple position as the refueling machine
was
repositioned to properly grapple the assembly.
The assembly
was then
moved to the upender
and on to the spent fuel pool.
Conclusions
The inspectors
concluded that the core offload was completed in a safe
and deliberate
manner.
It was noted that the amount of licensee
oversight
was adequate.
Inspectors
noted that activities associated
with a misgrappled fuel bundle were completed in a deliberate
and
safety-conscious.
manner.
Closed
LER 50-335/96-006-00
" Inadvertent
Loss of Containment Audible
Count Rate"
92901
This
LER was the result of the Unit 1 wide range audible neutron count
rate indication in containment
being temporarily rendered
during refueling operations.
The audible count rate is required
by TS
while in Mode 6 whenever core alterations
or positive reactivity changes
are in progress.
The loss of the audible count rate was the result of
the electrical
bus being deenergized
to support maintenance
on the bus.
Power was restored to the bus
and the audible count rate restored in
approximately five minutes.
The inspector
reviewed the licensee's
investigation of this event
and
the corrective actions identified in the
LER.
The cause of the event
was determined to be procedural
inadequacy
which did not identify the
audible count rate
as equipment that would be deenergized
when the bus
was
removed from service.
The inspector
reviewed the revised procedure
and found the guidance
adequate to identify the loads
powered from the
bus.
Additionally, the plant breaker list was revised to add detail of
the audible count rate for the specific breaker
and bus.
The inspector
reviewed this breaker list revision and other corrective actions
identified in the
LER and determined that they were satisfactory.
II. Maintenance
Conduct of Maintenance
General
Comments
62707
61726
Enclosure
2
a.
Inspection
Scope
12
The inspector
observed all or portions of the following maintenance
during the report period:
97015173
97002981
97017387
97031237
97017387
97024676
96032335
01 lA Low Pressure
Safety Injection pump routine
preventative
maintenance
01 Unit 1 Main Steam Safety Valve removal
01 Unit 1 High Pressure
Safety Injection preventative
maintenance
Ol 1A Component Cooling Water Heat
Exchanger
cleaning
01
1A High Pressure
Safety Injection pump routine
preventative
maintenance
01 Power Operated Relief Valve indication troubleshooting
01 Boric Acid Makeup Tank
1A Outlet For
Emergency
Boration
Also, the inspectors
observed
the following survei llances
and post
maintenance
tests:
OP 2-1400059 Reactor Protection
System
- Periodic Logic Matrix
Test
OP 1-0410024 Full flow testing of the Unit 1 Safety Injection
Tanks
b.
Observation
and Findings
The inspectors
found the work performed to be professional
and thorough.
All work observed
was with the work package
present
and in active use.
Technicians
were experienced
and knowledgeable of their assigned
tasks.
The inspectors
frequently observed
supervisors
and system engineers
monitoring job progress,
and quality control personnel
were present
whenever
requi red by procedure.
When applicable,
appropriate radiation
control measures
and Foreign Material Exclusion
(FME) controls were in
place.
The inspectors
considered
the work associated
with WO 96032335
01. to be
a particularly good example of a well planned
and executed
maintenance
activity.
The work area
was extremely clean with the tools laid out and
arranged for easy
use.
The system openings
were covered
and identified
by large signs
as
an
FME boundary.
The work package
was well written
and properly completed
up to the appropriate
step.
In addition,
see the additional discussions
of maintenance
observed
under M1.2, M1.3, M1.4,
and M1.5 below.
M1.2
Ins ection and Maintenance of lA Emer enc
Diesel Generator
62707
a.
Inspection
Scope
Enclosure
2
13
During the week of November 2, the inspector
reviewed the
1A Emergency
Diesel Generator
(EDG) inspection
and preventative
maintenance
activities.
The inspection included
a review of planned inspections,
. observation of inspections
in progress,
and observation of FHE controls.
Observations
and Findings
The licensee
had
a vendor
perform
a routine inspection
and corrective
maintenance of the
EDG.
The inspector
observed portions of the cylinder
inspections,
connecting
rod inspections,
bearing inspections.
and
fastener torque checks.
The inspections
found no problems with the
diesel.
The inspector also reviewed the applicable work orders
and
noted that the documentation of the findings was good.
One item of note,
was that the licensee treated the area
as
a level
2
FHE area.
According to thei r Procedure
QI 13-PR/PSL-2,
Revision 34,
"Foreign Material Control Housekeeping
and Cleanliness
Control Methods,"
an area
2 would be appropriate for systems
and components
where
configurations
and circumstances
allow foreign material to be
immediately retrievable
and
a final cleanliness
inspection to be
erformed.
The inspector
reviewed the requi rements
and found that the
icensee fully complied with the procedure.
Generic Letter 96-06 Thermal Pressurization
Relief Valve Installation
62707
Inspection
Scope
NRC Generic Letter identified
a potential
problem with thermally induced
overpressurization
of isolated water filled piping sections
in
containment jeopardi zing the ability of accident mitigating systems to
perform their safety related functions.
Florida Power
8 Light (FPKL)
identified three susceptible
piping penetrations
in Unit 1 that required
modification to prevent this potential
problem.
The inspectors
reviewed
the modification work packages
and observed portions of the modification
installation.
Observations
and Findings
The inspectors
reviewed the modification package,
PC/H 97032,
which
proposed to add
a thermal relief valve on each of three containment
The three penetrations
were in the non-safety related
containment
spray function.
They were P-46 and P-47, refueling cavity
pool purification supply and return lines,
and P-42, reactor cavity sump
pumps'ischarge
line.
The report adequately
documented
the design
change
and the justification that no unreviewed safety question existed.
On November
7, the licensee
informed the residents that the welders
who
would be performing this job had developed
a unique technique to weld
the
new valve bosses
onto the pipe while ensuring that
FHE was
Enclosure
2
14
maintained.
This technique
used
a leather 0-ring to seal
the prepared
pipe opening
from the inside.
They attached this to a clamping device
with an extra long bolt to allow retrieval if it fell into the pipe.
This clamping device held the boss in place until the root weld was
completed.
The leather provided adequate
strength to keep extraneous
material outside the pipe, but was flexible enough to insert in the
hole.
The valves were installed according to
PWO 61/2650 (P-42),
PWO 61/2652
(P-47),
and
PWO 61/2653 (P-46).
The inspector
observed the tack welding
and root welding for the valve on P-46.
The welders performed the
welding exactly as
seen in the shop
on November
7.
Also. the inspector
,verified that the welders were following the procedure
as written.
All
OC signatures
were noted to be obtained
.as required before continuing
the job.
En ineered Safet
Feature
Run of 1A Emer enc
Diesel
Generator
61726
Inspection
Scope
On November
12. the licensee
performed
a portion of Procedure
OP 1-
0400050,
Revision 46, "Periodic Test of the Engineered
Safety Features
ESF)."
The licensee
chose to perform
a fast start of the
1A EDG to
satisfy the post maintenance testing
and Technical Specifications 4.8. 1. 1.2.e.4
and 4.8. 1. 1.2.e.6 that required that the diesel
be started
each refueling by an
ESF test signal
and that the diesel
be run for 24
continuous
hours
each refueling.
The inspector
observed
the preparation
and start of the test.
Observations
and Findings
For the retest for the lA EDG, the licensee
performed part of the
Actuation System testing.
They had run the diesel that day as part of
the post maintenance test from the
EDG routine work just completed.
The
inspector
observed the pre test brief given by the Test Director and the
Operations
Supervisor.
The conduct of the brief included all applicable
precautions
and limitations.
The inspector
noted good participation
from the crew member s,
and noted that they raised several
valid
questions
during the session.
However, the brief was less than formal,
with several
conversations,
unrelated to the brief, taking place.
Two hours after the brief, conditions were established
to start the
test.
A question
was raised in the control
room about the need to roll
the engine before the test.
All the operators
knew that the diesel
did
not need to be rolled prior to this start since it had just been secured
four hours prior.
However,
none of the operators
could find where this
was permissible
by procedure.
The Assistant Nuclear Plant Supervisor
eventually found the note allowing this to occur in Appendix A of
Procedure
OP 1-2200050A.
Revision 35,
"1A Emergency
Diesel Generator
Periodic Test
and Operating Instructions."
Enclosure
2
't
15
The Test Director positioned her crew to perform the test.
Although
a
long period had expired between the brief and the beginning of the test.
the Test Director nor the
ANPS required another brief.
I&C personnel
input the Safety Injection signal
and the
EDG started
as expected.
The
inspector noted
good procedural
compliance
by the control
room personnel
during the start
and while loading the diesel.
The next day the load
run was successfully
completed
and the diesel
was secured.
Conclusions to Conduct of Maintenance
Maintenance activities were generally completed thoroughly and
professionally.
FHE control
was adequate
in all instances.
In one
instance.
the inspectors
found the installation of the thermal relief
valve in response
to Generic Letter 96-06 concerns
was completed
as
planned.
The inspector noted good procedural
compliance.
Also. the
inspector
found the technique
developed
by the we1ders to maintain
control to be innovative.
A portion of the
ESF Actuation System testing
was successfully
completed in spite of a less than formal brief by the
Test Director.
Re lacement
Pro ect
50001
Inspection
Scope
The inspectors
conducted walk-through inspections of the containment to
review preparations
for the
SGRP.
They also observed
clad-welding
activities involving the replacement
Obser vations
and Findings
The inspectors
observed
the following activities for the preparation of
removal of the existing steam generators:
~
Cleaning
and painting of the surfaces of the steam generators
to
encapsulate
contaminants.
Installing wedges in supports
and cables
around piping to minimize
movement of the main loop piping.
~
Preparations
for, and the final cutting and removal of the
containment construction
access
cover.
The activities observed
were being conducted in accordance
with
appropriate
work plans
and procedures.
During preparation
inspections of the steam generators,
the licensee
determined that the stainless
steel
cladding
on the primary nozzles
was
not thick enough.
The inspectors
observed
automatic
gas tungsten
arc
weld buildup activities on the cladding inside the primary inlet and
outlet nozzles.
These welding activities were found to be well
Enclosure
2
16
controlled, with the welders
and welding operators
aware of, and
following, appropriate
procedures.
Conclusions
Replacement
Project,
equipment
removal
and welding
activities were being conducted in accordance
with approved
plans
and
procedures.
Flow Accelerated
Corrosion
49001
The inspectors
reviewed the scope
and
a part of the inspection results
of the licensee's
program for monitoring
FAC in the steam,
condensate,
and feedwater
systems of St. Lucie Unit 1.
The scope of the inspection
included samples
selected
because of reported industry experiences
as
well as the samples
selected
from the licensee's
predictive program.
There were no major corrosion problems discovered
during these
inspections.
Based
on the sample
reviewed,
the licensee
continued to
maintain
a well-organized
program for monitoring flow accelerated
corrosion.
Inservice
Ins ections
73753
The inspector
discussed
the scope of inservice
and preservice
inspections
scheduled for the Unit 1 steam generator
replacement
outage.
During thi s report peri od, the
1 icensee
IS I inspectors
had spent the
majority of their effort doing wall-thickness
measurements
of piping in
support of the
FAC program,
and were just starting the scheduled
inspections.
The scope of the ISI and planned preservice
inspections
were appropriate.
Transfer of Unit 1 Incore Instrument
Remnants
62707
Inspection
Scope
Inspectors
reviewed the licensee's
planning for transferring
Incore
Instrumentation
(ICI) remnants
from the Unit 1 refueling pool to the
spent fuel pool.
Observations
and Findings
The licensee
removed several
ICIs from the reactor in preparation for
installation of new detectors.
The licensee cut the rhodium detector
segments off each ICI, and placed those pieces
in a disposal
container.
The remaining ICI segments,
approximately
12 feet long, were tied off to
the side of the refueling pool.
Measured
dose rates
on these
segments
were found to be 300 to 2500
mR.
To transfer the ICI remnants to the spent fuel pool, the licensee
constructed
a shielded transfer tube from the refueling pool through the
Enclosure
2
17
containment
emergency airlock.
An inspector
examined the transfer
tube,
and discussed
plans for the ICI transfer with licensee
personnel.
The
licensee
conducted briefings consistent with requirements
for
imfrequently performed evolutions.
including discussion of contingencies
for addressing
unexpected
conditions.
The inspector
concluded that the
activity was carefully and thoroughly planned.
The ICI remnant transf'er
was performed shortly after completion of the
core offload.
The activity proceeded
smoothly, with very low dose
absorbed
by workers.
Conclusions
The inspector
concluded that the transfer of ICI remnants
from the
reactor vessel
to the spent fuel pool was carefully and thoroughly
planned
and completed with low radiation dose
expended.
Maintenance
Procedures
and Documentation
SGRP Weldin
Procedures
50001
Inspection
Scope
The inspector
reviewed the welding procedure specifications
(WPS)
and
the supporting procedure qualification records
(PQR) for the St. Lucie
Unit 1 SGRP.
Observations
and Findings
The inspectors
reviewed fifteen WPSs which had been prepared
specifically for the St. Lucie
1 SGRP.
Thirteen of the procedures
were
qualified in accordance
with the requi rements of ASME Section
IX and
were supported
by PQRs;
two of the procedures
were prequalified
AWS
procedures
which did not require
PQRs.
For twelve of the
ASHE WPSs, the weld assemblies
represented
by the
were welded
and tested in 1997, specifically for the St Lucie SGRP.
The
review by the inspectors
showed that all required "essential"
and
"supplementary essential"
elements
were properly documented in the
and the
WPSs.
The remaining
ASHE
WPS (GT/8.43-1 SL) was
a gas tungsten
arc welding
procedure for welding stainless
steel to Inconel; the
PQR supporting
this
WPS
(PQR GTM/8.43-Ql, Rev.0)
was completed in February
1992.
and
reported the tests that were conducted in July 1985.
While the test
weld data
were in excess of 10 years old, the
PQR met all procedure
qualification requirements of the current
ASME Section
IX, in that, all
"essential"
and "nonessential"
welding variables
were provided by the
PQR.
Enclosure
2
M5
M5.1
18
The inspectors
did note that f'r two of the
WPSs
a nonessential
element
was not completed in two cases.
The procedures
for welding Inconel
(P43) to Carbon Steel
(Pl) and Inconel
(P43) to Stainless
Steel
(P8)
contained
"none" or "N/A" in the spot reserved for the weld filler
material
"A-number designation"
even though the materials
were fully
identified by brand
name in another part of the
WPS.
(In that the
has not assigned
an "A-number designation" for the Inconel welding
material
used,
accepted
protocol would have been to: list the filler
material
brand
name in the "A-number designation"
space of the
WPS,
rather than list it in another location.
The "A-number designation" is
listed as
a "nonessential
element"
by ASME Section
IX. and is required
to be included in the procedure.).
When this was pointed out. the
licensee/contractor
agreed to revise the two procedures
to show the
filler material
brand
name in the proper location in the
WPSs.
The inspectors
also questioned
the
PQRs for welding of "impact tested"
Pl materials.
The test assembly
base materials in the
PQR were listed
as "Pl,
Gp
1
& 2" to "Pl,
Gp
1
& 2" despite the tact that
a change
from
one group number to another would require requalification of the welding
procedure.
(As specified
by ASME Section
IX, to fully qualify with one
test plate, the assembly
would have to consist of Group
1 material
welded to Group
2 material.)
When this was questioned.
the
licensee/contractor
was able to produce
a material certification for the
test plates,
showing that the
ASME SA516,
Grade
60, test plate material
met all of the chemical
and physical
requi rements for ASME SA516,
Grade
70,
and therefore qualified as Pl, Group
1 and Pl, Group 2.
Conclusions
The welding procedures
for the Steam Generator
Replacement
Project were
complete
and appropriately qualified in accordance
with required welding
standards.
Maintenance Staff Training and Qualification
SGRP Welder
uglification
50001
Inspection
Scope
The inspector
reviewed welder qualification facilities and activities
related to preparations
for the
SGRP.
Observations
and Findings
The
SGRP welder training and qualification facility was
a converted
maintenance
building, outside the security area,
on the north side of
the St Lucie site; the facility was referred to as "the boathouse."
The inspector
reviewed the procedures
for security of welder
qualification test assemblies
through
a walk-through inspection with the
Enclosure
2
19
test
super visor
.
The inspector
was
shown
how welder identification was
verified; how test assemblies
were permanently identified;
and
how the
assemblies
were secured
in a locked
room when
a test weld took longer
than one shift to complete.
The supervisor
also demonstrated
how- the
test assembly identification was transferred to each
bend specimen
taken
from the assembly.
Conclusions
Replacement
Project welder training and qualification
activities were being conducted in full compliance with ASME Section
IX
requirements.
Quality Assurance in Maintenance Activities
ualit
Re orts and Surveillances
50001
Inspection
Scope
The inspector
reviewed quality and nonconformance
reports related to
welding activities.
Observations
and Findings
Quality reports
are generated
by the
FP8L Nuclear Assurance
Group to
document survei llances of licensee
and contractor
SGRP activities.
Since
Hay 1997, there
have
been in excess of 30 Nuclear Assurance
survei llances of the contractor's
welding related acti vities.
Twelve of
these surveillances
identified potential
problems with the
implementation of the welding program.
The inspector
reviewed the
12 surveillance reports that identified
unsatisfactory
audit findings.
The majority of the surveillance
findings were minor findings which were corrected at the time of
discovery
and reported in the surveillance reports
as
"VIS"
(unsatisfactory,
immediately satisfactory)
or were quickly corrected
after the surveillance
report was issued.
The results of these
surveillances
indicated that the welding program was functioning in a
satisfactory
manner, with only minor problems.
The major exceptions to this impression
were the findings of Quality
Reports
97-6186,
dated October
28,
1997,
and 97-6215.
dated October
30,
1997, which documented
problems with undersized
welds which had been
accepted
by the contractor's
QC inspectors.
The corrective actions for
these survei llances
involved 100 percent reinspection of welds accepted
by the
QC inspectors identified in the surveillance reports,
along with
a sample of welds accepted
by other
QC inspectors.
After the ultimate
disqualification of one
QC inspector,
the licensee
and contractor
concluded that they had determined the extent of the problem,
and had
corrected it.
The inspectors
agreed that the most serious
aspect of the
Enclosure
2
20
problem had been
addressed
by fully investigating the
QC inspector
involvement,
and that the corrective action was appropriate.
The one
question that did not seem to be addressed
was the welder and welder
supervisors'nvolvement
in undersized
welds that were turned over to
for inspection.
Conclusions
The licensee's
Nuclear Assurance surveillance activities provided
a
comprehensive
review of the contractor's
welding and welding inspection
activities.
III. En ineerin
Conduct of Engineering
Review and Walkdown on
SGRP Liftin
and Trans ort Pre aration for Unit 1
~50001
Inspection
Scope
The inspectors
examined the Steam Generator
Replacement
Project
(SGRP)
lifting equipment which was erected
inside
and outside the Unit
1
Containment Building.
Additionally, the inspectors
reviewed the
adequacy of the
SGRP lifting and transport
programs,
procedures,
work
packages
(WPs)
and load test records, to assure that they were prepared
and tested in accordance
with regulatory requirements,
appropriate
industrial codes,
and standards.
Observations
and Findings
The licensee contracted
the entire
SGRP to the Steam Generator
Team
(SGT) which was formed by a collaboration
between
Duke Power Engineering
(DPE) and Morrison Knudson Corporation
(MKC).
Duke Power Engineering
provided the engineering expertise
and
MKC provided the construction
'xpertise
to the project.
The
SGT subcontracted
the heavy lift
engineering
and operation of the
SGRP to Mammoet Transport Engineering,
Netherland.
The licensee listed American National Standard Institute (ANSI) codes
as
references
in the
SGRP Lifting Program.
As specified in ANSI N45.2. 15,
"Hoisting, Rigging.
and Transporting of Items for Nuclear
Power Plants,"
1981. the licensee
performed
110 percent
load tests for the erected
Temporary Lifting Devices
(TLD) inside the containment,
Outside Lifting
System
(OLS) outside the containment,
and transporters
which transferred
the steam generators
to or from the temporary storage
area.
A Horizontal Transfer System
(HTS) was installed inside the containment
and extended outside the containment
and provided the transfer
connection
between the TLD and the
OLS.
Enclosure
2
21
The licensee established
procedures
and
WPs, drawings.
and calculations
for removing, transporting,
and installing the original and replacement
SGs.
The inspectors
randomly selected
and partially reviewed the
following WPs, calculations,
and drawings for the heavy load lifting and
transport preparation:
WP 1039,
"Erection of TLD Mock-Up and Load Test of TLD and Gantry
Crane," Revision
0
Calculation
PSL-1MHC-95-014.
"Foundation Design for Temporary
Gantry and Horizontal Transfer
System for SGRP," Revisions
2 and
6
'FPL Dwg. SGR-DP-5.3-014,
"Handling
Containment,"
Revision
0
FPL Dwg. SGR-DP-5.3-016,
"Handling
SG Inside Containment-
Downending Process,"
Revision
0
FPL Dwg. SGR-DP-5.2-002,
"Handling Steam Generator Outside,"
Revision
1
The licensee successfully
performed the required load tests
in
preparation for the
as recorded
on
WP 1039.
The design loadings of
the foundations
were obtained
from addendum to this calculation,
and
included dead, live, and wind loads applied to the structures
and
foundations.
Three drawings detailed the
SG lifting, downending,
and
moving processes.
The inspectors
walked down and inspected
the lifting equipment stored in
the yard area,
the TLD erected
inside the containment,
the
OLS erected
outside the reactor building,
and the on-site fabrication facility for
performing final preparation of the steam generators.
The inspectors
considered that the erected lifting systems,
the on-site fabrication
facility, and the lifting equipment storage
area
were adequate
and could
achieve the intended function for the
SGRP.
A11 the temporary lifting
devices
and equipment will be removed from the site after the completion
of the
SGRP.
Conclusions
The inspectors
concluded that the required lifting plan. path,
calculations,
and analyses
generated
and performed for the safe lifting
and transfer operations
for the original and replacement
SGs were
adequate.
Review and Walkdown on
En ineerin
Pre aration for Unit 1
50001
Inspection
Scope
The inspectors
reviewed the installation of temporary pipe restraints;
Enclosure
2
22
modification of the existing restraints:
removal of snubbers,
beams.
instrument lines;
and pipe cuts in order to verify that the engineering
preparation for the removal of SGs
was in accordance with the applicable
WPs and drawings for the
SGRP.
b.
Observations
and Findings
The inspectors
discussed with the licensee's
engineers
the restraint
systems to be installed or modified for removal
and installation of the
SGs.
The licensee's
engineers,
based
on their research,
indicated that
there was
no evidence that any pipes
or
SGs would shift during or after
cutting.
However, the licensee
took precautions
and either installed
temporary restraints
or modified existing restraints to become rigid
restraints
in order to provide additional stability and prevent the
shifting of pipes during the cutting process.
This was done for the
SGs,
hot and cross leg pipes,
feed water pipes.
and
pipes.
The inspectors
reviewed several
WPs and drawings for installation,
modification,
or
removal of the restraints
and pipes
and considered
them
to be acceptable.
The inspectors
inspected
the preparations
for
removing the
and compared the work performed to the drawings.
The
inspected
elements
included pipe cuts, installation of the temporary
restraints,
modification of the existing restraints,
and removal of the
interferences
such
as
beams,
instruments,
and electrical
cables.
etc.
The drawings
used for the walkdown inspection were:
~
SGR-DP-6. 1.1-001 to 007,
Reactor Cooling System
- 1A side
~
SGR-DP-6.2. 1-001
and 002,
Main Steam Spring Hanger
MSH-79 and
Rupture Restraint
RE-MS-17 for SG
1A
~
SGR-DP-6.3.1,
Feed
Water Spring Hanger
BFH-81 and Rupture
Restraint
RE-BF-10 for SG
1A
~
SGR-151-193-001 to 006,
1A Piping Demolitions
The inspectors
found some minor discrepancies
during the walkdown.
These minor discrepancies
were discussed
with the appropriate
licensee
personnel.
The inspectors
considered that the engineering
preparation
for the removal of the
SGs was adequate.
c.
Conclusions
The inspectors
concluded that the licensee
performed adequate
engineering
preparations
for the removal, installation, modification of
piping, restraints
~
and interferences
for the removal
and installation
of the SGs.
Enclosure
2
23
El.3 Observation of SG Liftin
and Trans ortin
for Unit 1
50001
a.
Inspection
Scope
The inspectors
observed the lifting of the
SGs to and from the
containment
area
and transporting of the equipment to and from the
temporary storage
area to verify that those activities were performed in
accordance
with the established
procedures
or WPs.
.
Observations
and Findings
The
WPs used for the lifting and .transporting the original and
replacement
SGs were:
~
WP 2570A,
"Removal of Original Steam Generator
1A," Revision
1
~
WP 25708,
"Removal of Original Steam Generator
18," Revision
1
~
WP 3040A. "Installation of Replacement
1A,"
Revision
1
The inspectors partially observed
the licensee's
removal of two OSGs
from the containment
area
and transporting
them to the temporary storage
area.
The lifting and transporting
steps for the
SGs included:
checking
the clearances f'r removal; lifting and rotating the
SGs from the rest
pad to the center of the containment;
lowering the
SGs for sealing
(or
welding) the hot and cross
leg nozzles with cover plates;
downending the
a skid unit; pushing the
SGs outside containment;
lifting the
SGs to the transporter
by using the OLS: and transporting
the
SGs to the temporary storage
area.
For
a
RSG to be moved into the
containment,
the process
was reversed.
On November
15, the licensee
began lifting the
1A SG from its cubicle.
The lift was halted after the
SG was lifted approximately
2 feet,
so
that the remaining water could be removed from the channel
head.
It was
then raised
up to the refueling floor where covers were welded over the
hot and cold leg nozzles.
The
SG was then
moved outside of containment,
lowered to the mobile transporter,
and on November
18, transported to
the temporary storage location outside of the protected
area.
The 18 SG, which followed the same sequence
of events,
was lifted on
November
17 and transported to the temporary storage location on
November
19.
The inspectors
observed
a large portion of each aspect of the
SG move.
On November
16, the inspector
reviewed the procedure
being used to lift
the
Work Package
2570 A, Revision 1.
"Removal Of
Original Steam Generator
1A", and noted that several
steps
had not been
signed
as complete,
although the work had been performed.
The steps
not
signed were for the
SG to be hoisted
upward and then rotated
around
Enclosure
2
24
containment to align it with the equipment
hatch.
At the time the
unsigned
steps
were identified, the
SG was stationary with the
nozzle plugs being welded into place.
The inspector
brought this to the
attention of the
FP8L shift manager,
who had the procedure
updated.
In
addition, the inspector discussed this issue with both
FP8L management
and Steam Generating
Team
(SGT) management
to determine
what the
expectation
was with regard to signing off procedural
steps after they
are completed.
Although both groups indicated that. it was their
expectation that procedure
steps
be signed
as
soon
as possible after
they were complete,
QC offered several
explanations
why these
articular steps
were not signed.
One explanation
was that it would not
e safe for the Person
In Charge .(PIC) to divert his attention to
signing
a procedure
when the
SG was being moved.
Another explanation
was that the PIC was directing other important activities.
The
inspector took exception to these explanations
based
on the lack of
activity which was in progress
when the unsigned
steps
were identified.
Later inspections
did not identify additional
examples.
Overall, the inspectors
considered that the licensee
handled the removal
of the
OSGs very well.
During the welding process,
the inspectors
observed that the licensee
issued hot work permits
and stationed fire
watches with extinguishers
near the welding area f'r the control of
combustible materials
as required
by WPs.
The inspectors
also partially observed transporting
a
RSG from the
temporary storage
area
and lifting it into containment
and noted
no
discrepancies.
Shortly after lifting the first
OSG from its rest position, the
inspectors
went to the top of the TLD main girders
and f'ound that there
were no markings
on the top of the main girders to indicate the
hydrajack near side
and far side travel limits.
There were near side
and far side travel limit markings
on one side of one main girder and
there
was
a near side travel limit marking on the bottom of both main
gi rders.
Step 38, Sheet
14 of 17, of WP 1038,
"Erection of the
Temporary Lifting Device (TLD) inside the Containment." stated:
"Apply. or verify, markings (e.g.
~ tape line) on the top and
bottom of one of the main girders to show the travel limits from
the centerpost
centerline.
Note:
Ensure the locations of the
markings are visible to the hydrajack operator
and to the PIC on
the floor."
The inspectors
conducted
several
discussions
with a day shift PIC and
hydr ajack operator to verify they could see the
mar kings.
The
inspectors
also verified by di rect observations
the location of existing
main gi rder markings
and questioned if they could clearly be observed
for various main girder positions.
The inspectors
concluded that the
existing markings did not meet the
HP requirements
and they could not be
observed
from all main girder positions.
The licensee
marked the main
Enclosure
2
E2
E2.1
a.
25
girder as required
by the procedure
before the inspectors
concluded
their inspection in this area.
The lack of'arkings
on the top and bottom of one of the main girders,
such that the hydrajack travel limits were visible to the hydrajack
operator
and to the PIC on the floor, constitutes
a violation of 10 CFR 50 Appendix B, Criterion V. and the licensee's
accepted
Quality
Assurance
Program Section 5.0.
They collectively require that
activities affecting quality shall
be accomplished
in accordance
with
documented
instructions or procedures.
This was identified to the
licensee
as Violation 50-335/97-13-01,
"No Travel Limit Markings on the
.
Top and Bottom of One of the Main gi rders of the Temporary Lifting
Device."
Conclusions
Overall, the inspectors
concluded that the licensee
performed adequate
operations for the lifting and transporting of two OSGs from the
containment building to the temporary storage
area.
A violation was
identified for not marking the top and bottom of one of the main
girders. to indicate the travel limits of the hydrajack.
Engineering Support of Facilities and Equipment
Full Core Offload Safet
Anal sis
37551
Inspection
Scope
The inspector
reviewed the Engineering safety evaluation
PSL-ENG-SENS-
97-0050,
Revision 0, "Routine Performance of Full Core Fuel Offloads,"
to check technical
adequacy
and to ensure that all recommendations
had
been properly translated into procedures.
Observations
and Findings
Safety evaluation
PSL-ENG-SENS-97-050,
Revision 0,
was issued
by the
licensee
on August 19.
The purpose of the evaluation
was to develop the
conditions
under. which Unit 1 may fully offload the core for all future
refueling outages.
It also addressed
the temporary storage of the
reactor internals within the vessel
and the head
on the vessel
after all
fuel was transferred to the spent fuel pool.
The inspector
found the
evaluation well presented.
It clearly documented that no unreviewed
safety questions
existed.
Also, it laid the basis for future full core
offloads
as the routine.
The inspector
noted that
a
FSAR change
request
was included with the evaluation to agree that full core offload is the
normal
method of defueling.
Section 5.0 of the evaluation listed eleven conditions with which the
plant must comply in order
for the evaluation to be valid.
The
inspector verified that all of the restrictions
had been incorporated
Enclosure
2
E2.2
26
into the appropriate
procedures.
One item of interest that the
inspector
noted was that the procedure
revisions were not issued until
a
few days prior to the beginning of the outage.
The licensee
stated that
this occurred
due to the large workload for the Procedures
group.
The
inspector did observe that Operations
had
a dedicated
SRO reviewing the
procedures
as they became available to verify that the procedures
were
accurate.
Conclusions
The full core offload safety evaluation
was well presented
and clearly
documented
the lack of any unreviewed safety questions.
The evaluation
was properly translated into the applicable procedures to ensure that
the evaluation
was valid.
Flow Test of the Unit 2 to Unit
1 Condensate
Stora
e Tank Cross-tie
37551
61726
Inspection
Scope
The inspector witnessed the performance of LOI-0-85, Revision 0,
"Flow
Test of the Unit 2 to Unit 1 Condensate
Storage
Tank Cross-tie."
The
procedure
was
an "approved for use" copy of Revision 0.
Observations
and Findings
A cross-tie line between the Unit 2 Condensate
Storage
Tank (CST),
and
the Unit
1 CST,
was established
as part of a licensing commitment for
Unit 1.
The cross-tie
and dedicated
water supply in the Unit 2 CST were
provided for use in the event that
a vertical tornado missile disabled
the Unit 1 CST.
Inspector Followup Item 50-335/96-201-06,
was identified during an
NRC
design inspection.
documenting that although the cross-tie
had been
established, it had never
been flow tested.
In response,
to that
finding, the licensee
developed the aforementioned
procedure to operate
the Unit 1 Auxiliary Feedwater
(AFW) pumps through the cross-tie
from
the Unit 2 CST.
The purpose of the procedure
was to verify that the Unit
1 AFW accident flow rate plus the recirculation flow, could be passed
through the cross-tie.
Prior to performing the test,
the licensee
held
a pre-job brief.
The
inspector witnessed the brief and thought it to generally
be thorough.
It was attended
by the appropriate
personnel,
with the exception of the
non-licensed field operator.
The ANPS stated that he would be stationed
with the field operator
and would ensure
he received
an appropriate
brief, as needed.
During the briefing, it was identified that the
procedure
required
AFW flow to reach
460 gpm, but the range of the
control
room indicator
was only 400 gpm.
The licensee
reviewed the
engineering
analysis
and verified that operating the
pump at 400
gpm
Enclosure
2
E8
E8. 1
27
would be adequate to verify proper operation.
The procedure
was revised
and
FRG reviewed.
The inspector
reviewed the analysis
and concluded the
licensee's
conclusions
were sound.
The inspector witnessed portions of the pre-test
valve alignment
and
noted the operators verified each valve tag prior to manipulating the
valves.
Additionally, the inspector
noted that the oil level for the
1A
pump was below the normal level designated
on
a placard attached to the
pump skid.
The licensee
was informed and concluded that it was adequate
for operation of the pump.
The 1A pump was started, test data
was taken
and all the test criteria
were satisfactorily
met.
IFI 50-335/96-201-06, will remain open pending
an engineering
review of the test data.
Conclusions
The AFW cross-tie flow test
was satisfactorily completed.
The inspector
considered
the failure to identify the range of the flow meter to be
inadequate for the test,
a weakness
in the technical
review of the
procedure.
Hiscellaneous
Engineering Issues
Evaluation of Ino erable Unit 2 Containment
Fan Cooler
37551
Inspection
Scope
The inspectors
reviewed
an evaluation
performed
by the vendor,
Asea
Brown-Boveri Combustion Engineering Nuclear Operations
(ABB CENO), which
analyzed the significance of operating with an inoperable containment
cooling fan.
This evaluation
was performed in response to the licensee
discovering
one of the Unit 2 containment
fan coolers rotated in the
reverse direction when operated
in the emergency
mode.
The inspector's
review was performed to verify that the accident analysis
data
used in
the evaluation
was bounded
by that used in the
FSAR analysis.
The
details of this event were discussed
in Inspection Report 97-15.
Observations
and Findings
As discussed
in IR 97-15, the licensee
requested
that
ABB CENO evaluate
the safety significance of power operations with an inoperable
containment
fan cooler.
This evaluation
was
documented
in an ABB CENO
letter dated October
14,
1997.
ABB CENO concluded that peak containment
pressure for the limiting LOCA would increase
by no more than 0.5 psi,
and would not exceed
containment
pressure
design limits.
Inspectors
reviewed the ABB CENO letter,
FSAR Section 6.2,
and the
containment
fan cooler technical specification bases.
The limiting LOCA
for containment
pressure
is
a double-ended
suction leg slot
(DESLS)
Enclosure
2
28
break with minimum safety injection flow.
The event analysis
described
in the
FSAR was performed in 1993 as part of a licensee effort to
improve documentation of design basis information.
This case provided
the baseline
used for. the ABB CENO evaluation of the effect of an
containment
fan cooler.
After the
FSAR analysis
was updated in 1993, the licensee
asked
ABB CENO
to evaluate the effect of'
longer containment
spray delay time.
The
FSAR analysis is based
on the
TS delay time of 25.65 seconds,
which
represents
the time to start the containment
spray
pumps.
The licensee
calculated
a delay time of 45.5 seconds for flow to reach the spray
nozzles,
with full flow attained .at 58.5 seconds.
ABB CENO determined
that there
was sufficient margin in the calculation to accommodate
the
increased
delay time, so the peak pressure
reported in the
FSAR remained
valid.
ABB CENO subsequently
identified additional
conservatisms
in the
analysis,
and
recommended that
an updated
containment
response to a
be performed.
However, the conservatisms
identified by ABB CENO will
improve containment
pressure
margin for this event.
Therefore,
the
results given in the
FSAR remain bounding.
Conclusions
The inspectors
concluded that the evaluation
performed in response to
the discovery of an inoperable Unit 2 containment
fan cooler,
was
adequate
in that the accident analysis
data
used
was bounded
by the data
used in the
FSAR.
Additional discussion
and review of the inoperable
fan cooler was performed in
NRC Inspection Report 97-15 with EA number
97-501.
Closed
LER 50-335/96-014-00
"Invalid ESF Actuation of CI Oue to
Failed Rela
"
92903
This
LER documented
an invalid actuation of several
containment
isolation system
(CIS) components.
These actuations
resulted
from a
failed engineered
safety features
(ESF) actuation relay on October 27,
1996, for Unit 1.
There was
no adverse affect on plant operation.
The
relay was replaced
and the
ESF components
restored to their normal
operating configuration.
The inspector
reviewed the licensee's
investigation
and corrective
actions.
In addition to relay replacement
and system restoration,
additional corrective action included failure analysis of the relay and
a review of industry and plant data.
An adverse failure trend was not
identified for this relay.
Failure analysis identified the failure was
due to aging of the relay.
The inspector
found the licensee's
investigation thorough
and corrective action appropriate.
This
LER is
closed.
Enclosure
2
E8.3
E8.4
29
Closed
VIO 50-335/96-17-04
"Failure to
U date the Plant
Ph sics
Book"
~92702
This violation involved the failure to update reactor physics
data for
the Unit
1 Plant Physics
Curve Book.
Following completion of full
length control element'ssembly
(FLCEA) testing,
Verifications were performed
on October
31 and November
1,
1996.
Procedure
OP 1-0110055,
Revision 16, "Surveillance
Requirements
for
Modes
1 and
2 (Critical)," required operators to obtain
reactivity information provided in Figures A.6, B.3 and B.4 of the Unit
1 Plant Physics
Curve Book.
This Operator
Aid, as defined in Step 3.4.6
of Procedure
AP 0010140,
Revision 9, "Control of Operator Aids," is
"generated
and updated
by the Reactor Engineering department tor use by
Control
Room operators
in the operation of the plant."
The inspector
noted that the Unit 1 Plant Physics
Curve Book showed B.3 Reactivity
Deviation Log (Updated Monthly).
The last entry on Figure B.3 was dated
September
18.
The inspector brought this to the attention of the
ANPS who contacted
Reactor Engineering.
RE verified that Operating Surveillance
Procedure
64.01.
Revision
16,
"Reactor Engineering Periodic Tests,
Checks
and
Calibrations," Appendix 7, "Reactivity Deviation From Design,"
was
performed
on October
8 and not entered in the Unit 1 Plant Physics
Curve
Book Figure B.3 Reactivity Deviation Log.
Condition Report
No. 96-2751
was written to address this issue.
Procedure
QI 5-PR/PSL-l,
Revision 73, "Preparation,
Revision,
Review/Approval of Procedures,"
in Step 5. 14. 1 stated
"A strict
adherence to procedure/guideline
requirements
- Verbatim Compliance
- is
the policy expected
and required of all St. Lucie Plant personnel."
Procedure
OSP 64.01,
Revision 16,
"Reactor
Engineering Periodic
Tests'hecks
and Calibrations," Appendix 7, "Reactivity Deviation From
Design," Step 4. 15 stated
"Document the results in Plant Physics
Curve
B.3. Reactivity Deviation Log, in the Control
Room (applicable Unit) and
Reactor
Engineering Plant Physics
Curve Book."
The inspector
reviewed the root cause
and corrective actions identified
for this violation.
A verification checklist
was developed for updating
the Plant Physics
Curve book,
and the Reactor
Engineering
Schedule of
Periodic Tests
and Reports
AP-0010127
was revised to require
a weekly
review of the Plant Physics
Curve book.
The inspector
reviewed these
revisions
and found them adequate to correct the causes
of the
violation.
This violation is closed.
Closed
VIO 50-335/EA-96-457/03023
"Failure to Initiate
a Condition
Re ort for Labelin
on Safet
Related Detectors"
92702
This violation involved the fai lure of the I
8
C maintenance
personnel
involved in the replacement of the No.
6 Channel
B linear range detector
for the Nuclear Instrumentation to initiate a Condition Report
(CR) when
Enclosure
2
30
cables for the replacement
detector
were labeled differently than the
existing ones.
The inspector
reviewed the licensee's
cause determination
and corrective
actions for this violation.
The cause of the violation was determined
to be personnel
error
due to an informal approach
being used to resolve
the discrepant
condition instead of the requi red
CR process.
Personnel
were counseled
on the
CR process
and this violation.
The inspector
reviewed the
PHAI corrective action forms which identified the training
and the participants for this corrective action.
Additional corrective
action included documentation
provided by the vendor to clarify cable
designations.
The inspector
found these corrective actions
adequate
and
this violation is closed.
IV. Plant
Su
ort
Radiological Protection
and Chemistry Controls
Re lacement
Ins ection
50001
and Occu ational
Radiation
Ex osure
83750
Inspection
Scope
The purpose of this inspection effort was to verify that Radiation
Protection
(RP) activities for the Unit 1 Refueling Outage
(RFO) and the
Replacement
Project
(SGRP) were performed 'safely and met
applicable regulatory
and licensee
requirements.
The
RP program planning, preparation,
and implemented controls were
reviewed in the following program areas:
As Low As Reasonably
Achievable
(ALARA) planning:
Dose estimates
and dose tracking;
Exposure Controls
and temporary shielding;
Contamination controls;
Radiological
work plans
and controls;
storage
and disposal
and
Staffing and training plans.
The inspection included reviews of'ecords
and procedures,
interviews
with licensee
personnel
and observations
of work activities in progress.
The inspectors
made observations
in the Unit 1 Reactor
Containment
Building (RCB). Reactor Auxiliary Buildings
(RABs), Original Steam
Generator
(OSG) Interim Storage
Faci lity ( ISF),
and yard areas within
the Radiation Control Area
(RCA).
Observations
and Findings
Radiolo ical Work Plans
and
Enclosure
2
31
The
RP staff'egan
preparing for the
SGRP in 1996.
Approximately six
months prior to the start of the'outage
the licensee obtained the
services of radiation protection personnel
having experience
in recent
SGRPs to develop the specific ALARA work plans for the project.
The licensee
developed
a series of documents titled Health Physics
Project Overviews
(HPPOs) which provided Health Physics
(HPs)
an
overview of'he specific
SGRP and pressurizer
heater
replacement
tasks.
The
HPPOs described
the process
employed in the infrequently encountered
SGRP tasks
such
as pipe end 'decontamination
(RCS) pipe severance.
The documents
also outlined the application of
radiation protection measures
to be applied to processes
such
as the use
of containments
or High Efficiency Particulate Air-filters.
The
informative documents
served
as basic radiation protection plans for the
tasks.
The inspectors
reviewed radiological protection activities associated
with several
SGRP tasks during the inspection
and generally observed
the
application of sound radiation protection control measures.
The inspectors
reviewed the licensee's
dose goals for 1997
and the
to assess
thei r performance in obtaining those objectives.
The licensee
modified the various collective dose goals during the year.
The
original dose goals for 1997, the revised goals,
and actual
person-rem
accumulated
are
shown in the table below.
1997 SITE COLLECTIVE DOSE
GOALS AND ACTUAL EXPOSURE
(PERSON-REM)
Original
Goal
Routine Operations
25.0
Unit 2 RFO (Spring 97)
150.0
Unit 1
RFO (Fall 97)
205.0
Unit
1
240.0
Unit 1 Pressurizer
30.0
Plant Manager
Reserve
25.0
TOTALS
675.0
Revised
Goal
22.5
171.5
191.0
247.0
43.0
0.0
675.0
Actual*
Exposure
25.0
169.5
88.5
83.5
65.9
0.0
432.5
- Through day 29 (November
17,
1997) of the 75 day Unit
1
RFO and
The inspectors
reviewed the licensee's
processes
for estimating task
dose projections
and the licensee's
dose tracking system.
The licensee
was continuously
and effectively tracking and trending outage
and non
outage
doses to evaluate
dose reduction efforts on nearly 200 Radiation
Work Permits
(RWPs).
The total dose goal for all Unit 1 outage work was
481 person-rem.
Through
November
17,
1997 the actual
dose
was 238.0
person-rem
which was slightly above the projected
dose of 235.8 person-
rem.
The collective doses
were:
Enclosure
2
32
RFO ...........89.5
person-rem
vs projected
108.4 person-rem;
SGRP ..........82.5
person-'.rem
vs projected
100.4 person-rem;
and
Pressurizer
...65.9 person-rem
vs projected
27.0 person-rem.
With the exception of the pressurizer
heater
replacement
project the
licensee
was generally below the projected
dose estimates
for most
tasks.
In most of those,
the number of hours estimated for the tasks
turned out to be too low.
The licensee
underestimated
the time to cut
the heater
tubes which was one of the reasons
the pressurizer collective
doses
were so much higher than projected.
The inspectors
reviewed the results of the licensee's
shutdown
cleanup procedures
for the Unit
1 RFO.
The licensee
implemented
licensee
Procedure
COP-05.03,
Revision
1, "Refueling Shutdown/Startup
Guidelines."
The licensee
provided sufficient time in the outage
schedule for the cleanup
phase of the procedure.
The licensee
also
considered
the impact the crud burst would have
on various systems
and
delayed work in those areas until the clean
up processes
were completed
for ALARA purposes.
The
RCS clean
up process
worked as planned but did
not result in as great
a crud burst
as the licensee
expected.
However,
the licensee
reported the process
had reduced contamination levels in
the
RCS.
Ex osure Controls
and
Tem orar
Shieldin
On tours within the
RCA, the inspectors
made independent
radiation
surveys,
examined the adequacy of the licensee's
radiation protection
boundaries
and radiological postings,
examined labeling of containers,
verified radiation monitoring equipment in use
was calibrated
and
receiving periodic source
checks.
The inspectors
also checked the
security of high radiation areas,
housekeeping,
radiation worker
compliance with radiation protection controls,
observed
Health Physics
Technicians
(HPT) performing radiation surveys.
and inter viewed
radiation workers.
Overall,
RP controls were good.
The inspectors
found the licensee
made good use of remote monitoring
equipment including communication,
video and tele-dosimetry to reduce
collective dose.
The licensee
also utilized shielding when practical.
The licensee
reported using nearly twice as
much lead in the
SGRP outage
than used in previous outages.
Contamination Controls
Unusually large quantities of contaminated
materials,
tools and
equipment were utilized during the
SGRP.
The licensee
had prepared for
the handling of the materials.
The inspectors
observed
movement of tools and equipment out of the
licensee's
equipment
hatch throughout the inspection to verify proper
radiological controls were implemented for materials exiting the
Enclosure
2
33
Containment Building.
The licensee
had
a contaminated
area
boundary
that extended
outside the Containment Building approximately
30 feet.
The inspectors
found
a
HPT posted at the hatch at all times.
The
inspectors
noted the area
was not covered
and was exposed to the
elements.
The inspectors
inqui red about contamination controls
when
raining.
The floor of the contaminated
area
was covered with thick
plastic sheets
which sloped
down into a trough.
Licensee
representatives
reported during periods of rain, water
flowed into the
trough and was absorbed with mop heads.
The inspectors
asked
HPTs about
the ability to conduct contamination
surveys in the rain.
The HPTs
reported that release activities were halted during rain storms.
The
inspectors
observed
and reviewed area contamination
surveys
made at the
equipment hatch.
Contamination levels inside the contaminated
area
were
low and checked several
times each shift.
The
HPTs also surveyed the
clean side of the contaminated
boundary several
times
a shift.
No
violations of regulatory or licensee
procedures
were identified during
the review.
The licensee
opened the construction
hatch to permit the removal
and
replacement of the SGs.
The licensee
decontaminated
portions of the
RCB
and an area directly in front of the construction hatch.
The licensee
built a deck to support the track the
SGs travel
on in and out of the
RCB.
The licensee stationed
Health Physics
(HP) personnel
in the area
to control work activities there.
The area
was monitored for
contamination during the inspection.
The inspectors
also reviewed personnel
contamination reports
completed
in 1997.
The licensee
documented all personnel
contamination
events
when contamination levels greater
than
100 counts per minute/100
cm'ere
found on personal
clothing or body.
The inspectors
noted
many of
the contaminations
were the result of radiation workers adjusting face
shields or communication headsets.
No concerns with personnel
contamination
events identified.
During the review, the inspectors
observed radiation workers that were
entering contaminated
areas with protective clothing that was not fully
donned or sealed.
Workers were failing to zip coveralls
up fully or
close hoods.
When it was observed.
the inspectors
informed individual
workers or HPTs in the work area
and proper corrections
were promptly
made.
During the inspection,
the inspectors
noted
improved worker
performance
and increased
HP efforts to address
the observed
poor work
practices.
c.
Conclusions
The
HPPOs developed to instruct and establish
radiological controls for
unique
SGRP task were an excellent planning resource.
The inspectors
confirmed that
ALARA and
RP concerns
were factored into the
planning.
Collective dose for the pressurizer
heater project was
significantly underestimated.
With the exception of the pressurizer
Enclosure
2
R1.2
heater
replacement project, the licensee
was effectively estimating
and
tracking collective doses for planned tasks.
Good
RP control measures
were in place inside the licensee's
RCA and overall licensee
exposure
controls were effective.
Good use of'emote radiation monitoring
technology to monitor work in radiation
and to
save collective dose
was observed.
Licensee contamination controls were
effective.
Licensee
RP controls for temporary containment
openings
were
appropriate
and effective.
Radiation
Work Permits
50001
83750
Inspection
Scope
The
RP controls
as di rected
by
RWPs were reviewed to evaluate the
adequacy of the controls.
Radiation worker awareness
of those controls
was also reviewed.
Observations
and Findings
Licensee
RWPs provided instructions for radiation workers performing
task within the licensee's
RCAs.
As described
in section 12.5.3.4 of
the licensee's
Final Safety Analysis Report,
RWPs define allowable
exposures;
stay times; anti-contamination clothing; respiratory
protection:
survey requi rements;
and special
precautions
or instructions
for the work to be performed safely, efficiently, and within the ALARA
commitment.
Radiation
Worker Performance
Each worker entering the
RCA was required
by licensee
procedures
to
determine the proper
RWP f'r the work activity planned
and location
where the work was to be performed.
The licensee's
automated
Access
Control System
(ACS) was used
by RP staff to control access
into and out
of RCA areas.
Personnel
entering the
RCA were requi red to have
a
RWP,
a
thermoluminescent
dosimeter,
and
a Digital Alarming Dosimeter
(DAD).
The ACS terminal required the worker to provide the
RWP number
and. to
confi rm they had reviewed the
RWP requi rements.
If the
RWP requi red
a
pre-job briefing, the system would check to see if the worker had
attended
an applicable pre-job briefing and verify the radiation
worker's remaining allowable dose
was sufficient for the limits
specified
on the
RWP.
Each
RWP had
a dose limit per entry and
a dose
rate limit for the radiation worker.
The
DAD was set to alarm at those
values.
The
ACS monitor provided the
RWP user with the dose limit per
entry, the maximum dose rate field the worker was permitted to enter,
and the radiation worker's personal
remaining allowable dose limit.
During the review
NRC inspectors
observed radiation worker awareness
of
RWP requirements
was inadequate.
Technical Specification (TS) 6.8. l.a required written procedures
be
Enclosure
2
35
established,
implemented,
and maintained covering the activities
recommended
in Appendix A, Regulatory Guide 1.33, Quality Assurance
Program Requirements
(Operation),
Revision 2, February
1978.
Appendix A
paragraph
7.e required,
in part, the licensee establish
procedures
for
(1) Access Control to Radiation Areas Including
a Radiation
Work Permit
System
and (7) Personnel
Monitoring.
Section 3.5.2 of the licensee's
Health Physics
Procedure
(HPP)-2,
Revision
10. "Florida Power and Light Health Physics Hanual," requi red,
in part, prior to using
a
RWP. workers should read
and understand
the
RWP requirements,
document that they have read
and understood
the
RWP,
and agree to comply with their requirements.
Personnel
were not
permitted to deviate
from the requirements
of the
RWP.
Section 5.9 of HPP-1.
Revision
10, "Radiation Work Permits," required,
in part,
a job specific
RWP for entry into the
RCB.
Additionally,
section
5. 10, required'n part.
any individual entering
an area
where
an
RWP is required should
be aware of special
instructions
and remarks
listed on the
RWP.
The licensee's
RWPs list the entry radiation dose
limit and radiation dose rate limit in the Special
Instructions section
of the
RWP.
The
ACS set the workers
DAD alarm setpoints
as specified
on
the
RWP.
The inspectors
observed
a radiation worker in the
RCB that was asked
by
an
HP. controlling work in the area, to identify the specific
RWP the
worker was using.
The worker reported using
a 500 series
RWP.
The
informed the worker that the 500 series
RWPs specifically excluded their
use in the
RCB.
The radiation worker was required to exit the
RCB.
The
worker had entered the
RCB on
a
RWP for the
RAB.
Licensee
RWP 97-1431,
Rev 0,
was written for pressurizer
heater
replacement
work in the Unit 1
RCB 18oot elevation
and pressurizer
platform area.
The
RWP set
an entry dose limit at 300 mrem and
a dose
rate alarm at 1,000 mrem/hr.
While observing
RP activities in the
RCB,
a
HPT providing
HP job
coverage of the pressurizer
heater
replacement activities asked
a
radiation worker about his radiation dose limits specified
on the
(97-1431) the worker
was using.
The technician wanted to know what dose
limit was specified
on the
RWP and shown on the
ACS terminal.
The
radiation worker reported that
he did not know what the
RWP dose limit
was.
The inspectors
brought the problem of radiation worker knowledge
and
awareness
to the attention of HP management.
Management's
response
was
timely.
An informal survey of a large population of radiation workers
in the
RCA and others entering the
RCA was
made by the licensee's
staff.
Host of the radiation workers could not answer correctly,
questions
concerning the
RWP requi rements they were requi red to review
and
know prior to work in the
RCA.
The
HP department
immediately
Enclosure
2
36
assigned
monitors at Containment Building and the Containment
Access
Building (CAB) to verify the radiation workers were using the correct
RWP.
knew what their personal
remaining allowable dose was,
and
knew the
RWP specified
dose per entry and
maximum dose rate limits.
Monitors and
HP staff reported radiation worker performance
improved rapidly within
24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.
During following reviews, the inspectors
found that radiation
worker knowledge of individual remaining allowable dose,
dose per entry,
and maximum allowable dose
improved significantly and was later
satisfactory.
Failure of radiation workers to utilize the correct
RWP for entering the
RCB and failure of radiation workers to maintain awareness
of RWP
requirements
concerning specified
dose limits were identified as two
examples of a violation of licensee
RP procedures.
VIO 50-335.389/97-13-
02,
"Inadequate
Radiation Workers Awareness of RWP Requirements."
Pressurizer
Radiation Protection Job Covera
e
Licensee
TS 6.8. 1.a required that written procedures
be established.
implemented,
and maintained covering the activities
recommended
in
Appendix A, Regulatory Guide 1.33, Quality Assurance
Program
Requirements
(Operation),
Revision 2, February
1978.
Appendix A
paragraph
7.e requi red licensee establish
procedures
for (1) Access
Control to Radiation Areas Including
a Radiation
Work Permit System
and
(7) Personnel
Monitoring.
HPP-3, Section 7.2 listed responsibilities of HP personnel
covering work
in High Radiation Areas including, in part,
knowing the requirements of
the
RWP including any special
precautions that
may be necessary
for
entry into the area
and maintaining control of and authority over
workers in the area.
While observing work in progress,
the inspectors
spent
some time at the
pressurizer
heater
replacement
control point in lower containment.
The
HPT at the station
had just received
a turnover
and was observing the
radiation workers below the pressurizer with remote video and dosimetry
monitoring systems.
The workers
on the pressurizer
platform were
cutting the heater
tubes
and were wearing tele-dosimetry to permit
continuous
and remote monitoring of their individual radiation doses.
The tele-dosimetry monitor system displayed the radiation dose
information for each worker in the area
on top of the video.
The
workers were receiving dose at
a rate of several
hundred mrem/hr.
As
one worker 's dose
approached
300 mrem
a series of four blocks
began to
turn red one at
a time.
The inspectors
questioned
the
HPT about the
significance of each
red block.
The HPT knew the indicator
meant the
worker was approaching
a dose limit but could not explain the
significance of each
red block.
The
HPT had been told in a turnover
that the dose per entry had been raised
from 300 to 400 mrem per entry.
However, the
HPT did not have
a copy of the
RWP 97-1431 at the
checkpoint.
The blocks for one of the workers continued to turn red as
Enclosure
2
37
the worker 's dose neared
280
mrem of dose.
The
HPT made several calls
to confirm the dose limit had been raised
from 300 to 400 mrem.
When
the dose for one worker approached
290 mrem the
HPT pulled the workers
out of the work area.
The radiation doses
received
by the workers cutting and removing the
heater
coils were higher
than expected
and the radiation workers were
quickly approaching
the 300 mrem dose limit originally specified
on
97-1431.
To improve efficiency and increase
worker stay times
on the
pressurizer
platform a decision
was
made by the
HP staff to increase
the
entry dose from 300 mrem to 400 mrem/entry.
The
RWP was revised to
reflect the change.
The inspectors
learned the data
base for the
RWP system
and the tele-
dosimetry monitoring systems
were not connected.
When an
RWP dose limit
changed
and workers were issued tele-dosimetry it was necessary
for the
HPs changing the
RWP to communicate those
changes
to the
HPs issuing the
tele-dosimetry.
On November
4,
1997,
HP personnel
raised the entry dose
limit on
RWP 97-1431
from 300 mrem to 400 mrem without notifying the
persons
issuing tele-dosimetry.
As
a result,
workers having
an entry
limit of 400 mrem were assigned
dosimetry that was set to alarm at 300
mrem.
The radiation monitoring system
on the HPT's video monitor was
operating with the 300 mrem dose limit instead of the 400 mrem dose
limit specified
on revision
1 of RWP 97-1431.
That was the reason the
visual alarm indicator (series of four red blocks)
was peaking at
a dose
of about
290 mrem.
The
HPT acted conservatively
and pulled the radiation workers out of the
area
and no administrative
dose limits were exceeded.
However, if the
dose limits had been
lowered instead of raised
and the persons
issuing
the tele-dosimetry were unaware of those
changes
the alarm system
on the
dosimetry monitoring equipment would not have alerted the
HP to workers
approaching
or exceeding
a radiation dose limit.
The inspectors
concluded that the licensee's
RP procedures
were inadequate.
in that,
the procedures
did not describe the tele-dosimetry
issuance
procedures
and provide
a process to ensure
personnel
setting radiation monitoring
system setpoints
remained
knowledgeable of dose setpoints
modified when
RWPs were revised.
Failure of'he licensee to have written procedures
for the issuance of
tele-dosimetry that would ensure the dose limit setpoi nts applied i n
tele-dosimetry monitoring systems
were in agreement
with the limits
established
on the applicable
RWPs was identified as
a violation of the
licensee's
TS.
VIO 50-335.389/97-13-03.
"Failure To Have Adequate
Procedures
for Issuance of Tele-dosimetry."
Enclosure
2
-38
R1.3
Conclusions
Inadequate
radiation worker awareness
of RWP requirements
was
identified as violations of the licensee's
RP procedures
and licensee's
TS.
Inadequate written procedures
for the issuance of tele-dosimetry
and
setting dosimeter setpoints
in agreement with the
RWP requirements
was
identified as violation of licensee's
TS.
Control of Ver
Hi h Radiation Area
83750
Inspection
Scope
The purpose of this inspection effort was to review ci rcumstances
regarding failure to maintain positive
HP control of a posted
Very High
Radiation Area
(VHRA).
Observations
and Findings
Title 10 CFR Part 20 defines
a
VHRA as
an area,
accessible
to
individuals, in which radiation levels could result in an individual
receiving
an absorbed
dose in excess of 500 rads in 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> at
1 meter
from a radiation source or from any surface that the radiation
penetrates.
Title 10 CFR Part 20. 1602 prescribes
requi rements for access
to VHRA.
In addition to the requi rements in 20. 1601 the licensee shall institute
additional
measures
to ensure that
an individual is not able to gain
unauthorized
or inadvertent
access
to areas
in which radiation levels
could be encountered
at 500 rads or more in 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> at
1 meter
from a
radiation source or any surface through which the radiation penetrates.
Title 10 CFR Part 20. 1101 (a), requires
each licensee
develop,
document
and implement
a radiation protection program commensurate
with the scope
and extent of licensee activities and sufficient to ensure
compliance
with the provisions of this part.
Licensee
procedure
HPP-3,
Revision 3,
"High Radiation Areas", Appendix A
Definitions defines Positive Access Control
- f'r VHRA to include
locking with a lock and key unique to the area.
Health Physics
Procedure
HPP-24,
Revision 5,
"Containment Entries At
Power," described
requi rements
for securing
RCB hatches.
Form HPP-24. 1
Securing
From
RCB Entry required,
"Locking Devices
must be secured
such
that both locks (Security and Health Physics)
must be removed before
handwheels
can be operated."
The Security and
HP departments
each locked the handwheels to the
Enclosure
2
R2
R2.1
= 39
containment
hatches.
The licensee utilized one chain with both locks to
secure the hatch handwheels.
On October 8,
1997, licensee
personnel
found the
HP lock on the emergency
escape
hatch
on the Unit 2
Containment
Bui lding was not locked in such
a manner to prevent
access
to the Unit 2 Containment Building.
The
HP lock would not have
prevented
operation of the hatch handwheel.
Following the discovery the
HP lock was latched properly and the licensee initiated
a Condition
Report to cause
a review and corrective actions for, the identified
problem.
The licensee
chose to utilize two chains.
one for the security
and another for the
HP lock:
The corrective action should prevent
similar improper lock configuration.
While the improperly positioned
lock would not have prevented
access
into the equipment hatch.
the
equipment hatch
remained
secured with a lock controlled by the Security
department
at all times.
There was no evidence that anyone
had
improperly accessed
a
VHRA.
Access controls for VHRA are expected to be positively controlled as
access to such high radiation areas
(greater
than 500 rad/hr ) can be
life threatening.
This licensee identified and corrected violation is
being treated
as Non-Cited Violation,
NCV 50-335,389/97-13-04,
"Failure
to Follow Procedures
for Securing Access to a Very High Radiation Area."
Conclusion
A NCV was identified for failure to follow procedures
for securing
a
VHRA.
Status of Radiation Protection
and Chemistry Facilities and Equipment
SGRP Facilities and
E ui ment
50001
Inspection
Scope
To verify that
SG removal activities were performed in compliance with
regulatory
and licensee's
RP program requirements.
b. Observations
and Findings
To facilitate the processing of a large work force on site supporting
the
SGRP,
the licensee established
a
SGRP control point in temporary
facilities erected
on the north side of the site.
The facility included
an
HP checkpoint, briefing and video monitoring room,
HP office space,
a
dress-out facility, ACS,
and whole body personnel
contamination
monitors.
The inspectors
found the facility to be well equipped
and
performing the intended functions of a primary RCA control point and was
evidence of managements
support to the site
RP program.
Ori inal Steam Generator
Removal
Movement
Interim Stora
e and Dis osal
The inspectors
reviewed the licensee's
plans for removing the
OSG from
Enclosure
2
40
the
RCB,
movement of the
OSGs to the
ISF and plans for transporting
and
disposal of the
OSG.
The licensee
implemented effective measures
to remove water from the
OSGs,
seal
the
OSG ports,
and
remove
and seal
fixed contamination
on the
external
surfaces
of the
OSGs.
The licensee
established
effective
RCAs around the
OSGs
when they were
removed from the
RCB.
The movement of the
OSGs from the protected
area
to the
ISF was efficient, orderly,
and controlled to prevent unnecessary
radiation doses.
The radiological controls at the
ISF were well planned
and effective.
The inner and outer perimeters
were properly posted.
The inspectors
made independent
radiation surveys of general
areas within the OSG-ISF
and along the perimeters.
Radiation levels outside the inner radiation
perimeter were all less than
5 mrem/hour
and radiation levels outside
the outer
RCA perimeter
were all less than 0.2 mrem/hr.
The facility
was properly secured.
posted,
and controlled.
The licensee
planned to ship the
OSGs intact to a waste disposal
facility.
The licensee
had applied for exemption from the packaging
requi rements for a Surface Contaminated
Object
(SCO) required in
Department
Of Transportation
(DOT) regulation
49
CFR 173.427
and from
the
SCO limits in 49 CFR 173.403 in order to facilitate the one time
controlled shipment of two SGs from the St. Lucie site to Chem-Nuclear
Systems
Low Level Radioactive
Waste
Management Facility in Barnwell,
The request
was dated
June
19,
1997.
The licensee
received the exception
from the
DOT in a memorandum
dated
October
2,
1997.
The exception permitted the licensee to classify the
as
SCO
and transport the
SGs un-packaged
under
a transportation
plan that was
to provide an equivalent level of safety to the packages
and procedures
specified in the
DOT regulations.
The SGs were prepared for transportation
by cutting the penetr ations at
the primary cooling water inlet and outlet nozzles,
the secondary
feedwater nozzles,
the secondary
steam exit nozzles,
and several
instrumentation lines.
The penetrations
were to be sealed with welded
closures that also provide
some shielding of the radioactive material
inside.
Inspection ports
and manways
were covered
by bolted closures
that were
a part of the original design.
The SGs were to be shipped
by barge to the Savannah
River Site and by
land with a heavy haul
motor vehicle to the disposal facility.
The
licensee
had developed
an approved shipping plan for the process
and
planned to ship the generators
in 1998.
c.
Conclusions
The licensee
established
excellent
RP support facilities for the
Enclosure
2
V
R5
41
and good
RP controls for the removal
and movement of the
OSGs to the
ISF.
The licensee
was well prepared to ship the
SG to a disposal
facility.
Staff Training and gualification in Radiation Protection
and Chemistry
R5.1
S1
SGRP Staffin
and Trainin
50001
Inspection
Scope
Review adequacy of staffing and training for the
HP and radiation
workers for the
SGRP.
Observations
and Finding
The site had obtained
a sufficient number of HPT and support personnel
for the
SGRP.
On tours throughout the
RCA the inspectors
observed
good
HP presence
and
a sufficient number of HPTs to control work.
No
staffing concerns
were identified.
The licensee
developed specific training plans for radiation workers
and
HPls.
Radiation workers received training on the ALARA program relative
to the
SGRP which addressed
ALARA goals,
worker responsibilities
in
maintaining exposures
ALARA, site ALARA program processes,
general
dose
reduction guidance, site exposure tracking capabilities,
overview of
planned
dose reduction processes,
and site ALARA contacts.
Interviewed
radiation worker s were knowledgeable of maintenance
and modification
processes
employed during the
RFO and
SGRP.
The licensee
performed
mockup training on several
SGRP tasks to qualify
personnel.
The licensee
developed
approximately fifteen mockup training
modules for the
SGRP.
The licensee
addressed
RWP requirements for some
of the tasks
and students
were required to understand
the radiological
requirements
and conditions of the mockup activity.
Some staff personnel
participated in some mockup training for the
pressurizer
heater
replacement
project offsite.
However, licensee
personnel
reported that the mockup used
was not identical to the actual
plant configuration.
The licensee did not identify several
equipment
problems
and space restrictions
encountered
during the pressurizer
heater
removal at St. Lucie.
Conclusions
The
RP staffing levels were sufficient to provide good
RP support for
the planned outage activities.
Training activities for radiation
workers
and
HPTs working the
SGRP activities were appropriate.
Conduct of Security and Safeguards Activities
Enclosure
2
S1.3
Fitness for Out
Ins ection Sco
e
81502
42
S2
S2.1
The inspector
reviewed
random Fitness
for Duty (FFD) records
and reports
at St. Lucie and the Florida
Power and Light (FP8L) Corporate Office to
determine if the licensee
was in compliance with the provisions outlined
in 10 CFR 26.
Observations
and Findin s
The inspector
reviewed the following procedures
and selected
a random
number of records to review in conjunction to determine if the
licensee's
procedures
were being followed:
FFD-2, Revision 2. "Urinalysis Collection Instruction"
NP-400,
Revision 5, "Fitness for Duty"
FFD-5, Revision 3, "Processing
and Reporting Test Results"
DOC-2, Revision 1, "Protection of Confidential
Information/FFD Records Retention"
Conclusions
Through
a randomly selected
record review and discussions
with licensee
representatives,
the inspector determined the licensee
was following
their
FFD procedures,
which were in accordance
with 10 CFR 26.
Status of Security Facilities and Equipment
Status of Securit
Facilities
and
E ui ment
71750
Inspection
Scope
On October
19, the inspector walked down the protected
area barriers to
verify they were intact.
In addition, the posting of the requi red
NRC
forms was also verified.
Observations
and Findings
In performing these walkdowns, the inspector verified the fence fabric
had no unintentional
openings,
was not degraded,
and was not eroded at
the base;
isolation zones
were free of objects
and well illuminated;
and
compensatory
guard postings
were in place
as necessary.
The inspectors verified that all required
postings
were current.
Two
exceptions
were noted posted in break
rooms.
The licensee
determined
that these
were postings in excess of their procedures.
Subsequently,
the licensee
ensured that the postings
were hung in accordance
with
their procedure.
Enclosure
2
c.
Conclusions
43
The protected
area barriers
were in good condition, the isolation zones
well lit, and the appropriate
compensatory
guard postings in place.
S5
Security Safeguards Staff Training and Qualification
S5.1
General
Comments
81700
During the
NRC Chairman's visit to St. Lucie on November
17,
1997, it
was noted that security force personnel
were carrying weapons outside of
their cases.
The inspector noted that the licensee
had improved
Security Force Instruction 9, Revision 6, "Firing Range Operating
Procedure."
The licensee
now utilizes
weapon
gun cases to transport
one
or two weapons to the range.
If more than two weapons
are to be
transported.
they will be transported
in a security vehicle.
Additionally, the licensee
published
an Inter-Office Correspondence
-to
remind personnel
that long guns taken outside the protected
area
should
be cased at all times.
S8
Hiscellaneous
Security and Safeguards
Issues
S8.1
Re lacement
Ins ections
Ins ection Sco
e
50001
The inspector evaluated
the licensee's
implementation of compensatory
measures
in place during the steam generator
replacement
project.
Additionally, the inspector
reviewed access
control
and affected vital
area barriers during the course of the inspection to determine
compliance with the licensee's
Physical Security Plan
(PSP).
b.
Observations
and Findin s
The St. Lucie PSP,
Revision 49, dated
December
18,
1997, Section 3.3.6
~
states
in part that major equipment
assemblies
need not be searched.
Upon arrival
on Hay 7 and 8,
1997. the licensee
performed
a cour tesy
search of'elect portions of both steam generators.
The steam
generators
were placed in the protected
area to be stored.
During the
period of September
15-26.
1997. the licensee
performed
a limited search
of the generators
during the course of removing the sealed
packaging the
generators
arrived with.
Upon review of Security Information Reports
and discussions
with licensee
representatives,
the inspector
determined
that all searches
were conducted in accordance
with PSP commitments.
No discrepancies
were noted by the licensee with respect to the
integrity of the steam generators.
The inspector determined that
associated
vehicles
and .personnel
were appropriately searched.
The inspector
reviewed
and observed the licensee's
existing plan to
control access
during movement
and work on the steam generators
being
Enclosure
2
i
S8.2
X1
44
replaced.
The inspector identified that access
was appropriately
controlled to prevent unauthorized
personnel
and equipment
from entering
containment.
The inspector verified that vital area barriers that were removed
due to
replacement of the steam generators
were appropriately
compensated.
Other deficiencies in security systems,
such
as loss of Closed Circuit
Television
Cameras
(CCTV) due to blockage
by the steam generators.
were
also appropriately
compensated
according to the licensee's
PSP.
Conclusion
The licensee's
planned
compensatory
measures,
removal of vital area
barriers,
and access
control of'ontainment during the steam generator
replacement
project were appropriate
and met the requirements
specified
in the
NRC approved
PSP.
Action on Previous
Ins ection Findin s
92904
Closed
VIO 50-335 389/96-16-01
and 50-335 389/EA-96-458/01023
-Failure to Submit
a
Re ort Under
The licensee initiated corrective action in response to a failure to
report
a tampering event (96-16-01)
and to a failure to report
an actual
entry of an unauthorized individual into the protected
area
(EA-96-458).
The inspector
reviewed Security Procedure
0006125,
Revision
10,
"Reporting of Safeguard
Events."
and determined the procedure
was
adequately
changed to clarify the definition of tampering
and the
associated
guidance to make
a clear determination if reportability was
necessary
during the course of similar events.
Additionally, Security
Event Response
Guideline,
Revision 0. dated October
10.
1996,
was
developed to provide for action in response
to an event that resulted
from, or was suspected
to have resulted
from deliberate or malicious
actions against the plant.
In conjunction with this guideline,
an Event
Review Team gathers
when such
an event is suspected,
to investigate
and
provide rapid response to determine the root cause of plant events or
conditions.
The prospect of malicious or deliberate
actions or
suspected
tampering are factored in to better guide the licensee
on
a
course of action
and reportabi lity matters.
The inspector
reviewed the
licensee's
responses
dated October
18,
1996,
and February
6,
1997.
respectively to determine if the proposed corrective actions
by the
licensee
were appropriate.
The corrective actions are considered
adequate to close these violations.
V. Mana ement Meetin s and Other
Areas
Exit Meeting Summary
The inspectors
presented
the inspection results to members of licensee
management
at the conclusion of the inspection
on November
24,
1997.
Interim
Enclosure
2
45
exit meetings
were held on November 6, 20,
and 21,
1997 to discuss
the
findings of Region based
inspection.
Proprietary information was reviewed,
but is not contained in the report.
The licensee
acknowledged
the findings
presented.
PARTIAL LIST OF
PERSONS
CONTACTED
Licensee
H. Allen. Training Manager
C. Bible, Site Engineering
Manager
W. Bladow, Site Quality Manager
G. Boissy, Materials
Manager
H. Buchanan,
Health Physics Supervisor
D. Fadden,
Services
Manager
R. Heroux,
Business
Manager
H. Johnson,
Operations
Manager
J.
Harchese,
Maintenance
Manager
C. Marple, Operations
Supervisor
J. Scarola,
St. Lucie Plant General
Manager
A. Stall, St. Lucie Plant Vice President
E.
Weinkam, Licensing Manager
W. White, Security Supervisor
Other licensee
employees
contacted
included office, operations.
engineering,
maintenance,
chemistry/radiations
and corporate
personnel.
INSPECTION
PROCEDURES
USED
IP 37551:
IP 61726:,
IP 62707:
IP 71001:
IP 71707:
IP 71750:
IP 83750:
IP 92702:
IP 92901:
IP 92903:
~0ened
Onsite Engineering-
Inspection of Erosion/Corrosion Monitoring Programs
Replacement
Inspections
Surveillance
Observations
Maintenance
Observations
Licensed Operator Requalification
Program Evaluation
Plant Operations
Plant Support Activities
Inservice Inspection
Occupational
Radiation
Exposure
Followup on Corrective Action For Violations and Deviations
Followup - Plant Operations
Followup - Engineering
ITEMS OPENED.
CLOSED,
AND DISCUSSED
50-335/97-13-01
"No Travel Limit Markings on the Top and Bottom
of One of the Main gi rders of the Temporary
Lifting Device" (Section
E1.3)
Enclosure
2
50-335,389/97-13-02
50-335,389/97-13-03
50-335,389/97-13-04
Closed
50-335/96-006-00
50-335/96-014-00
50-335,389/96-16-01
46
"Inadequate
Radiation Worker Awareness of RWP
Requirements"
(Section R1.2)
"Failure to Have Adequate
Procedures
for
Issuance of Tele-Dosimetry" (Section Rl.2)
"Failure to Follow Procedures
for Securing
Access to a Very High Radiation Area
(VHRA)"
(Section R1.3)
LER
"Inadvertent
Loss of Containment Audible Count
Rate" (Section 08. 1)
LER
"Invalid ESF Actuation of CI Due to Failed
Relay" (Section E8.2)
"Failure to Report Event to NRC" (Section S8.2)
50-335/96-17-04
"Failure to Update the Plant Physics
Book"
(Section E8.3)
50-335/EA-96-457/03023
"Failure to Initiate
a Condition Report for
Labeling on Safety Related Detectors"
(Section
E8.4)
50-335,389/EA-96-458/
"Violations Assessed
a Civil Penalty Related
01023
To Security Access.
Failure to Hake
a
NRC
Notification Within One Hour
as Required
by 10 CFR Part 73" (Section S8.2)
Discussed
50-335/96-201-06
IFI
"Full Flow Testing of AFW Crosstie"
(Section
E2.2)
LIST OF ACRONYMS USED
ANPS
ASME Code
ATTN
CFR
As Low as Reasonably
Achievable (radiation exposure)
(system)
Assistant
Nuclear Plant Supervisor
Administrative Procedure
Annunciator Response
Procedure
American Society of Hechanical
Engineers
Boiler
and Pressure
Vessel
Code
Attention
Control
Element Assembly
Code of Federal
Regulations
Enclosure
2
CIS
CR
DWG
ENG
FLCEA
FPKL
FR
FRG
HPP
HPPO
HPT
HTS
I8C
ICI
ISF
LER
mrem
No.
NPF
NRC
NWE
OLS
OP
OSG
PMAI
PSL
PWO
-47
crating license)
rating license)
cation)
Enclosure
2
Containment Isolation System
Condition Report
Condensate
Storage
Tank
Demonstration
Power Reactor
(A type of op
Drawing
Enforcement Action
Emergency
Diesel Generator
Engineering
Engineered
Safety Feature
Flow Accelerated
Corrosion
Full Length Control Element Assembly
.
The Florida Power
8 Light Company
Federal
Regulation
Facility Review Group
Final Safety Analysis Report
Health Physics
Health Physics
Procedure
Health Physics Project Overviews
Health Physics Technician
Horizontal Transfer System
Instrumentation
and Control
Incore Instrumentation
Interim Storage Facility
InService Inspection
(program)
Job Performance
Measurement
Licensee
Event Report
milli rem
Non Cited Violation (of NRC requirements)
Number
Normal Operating
Pressure
Nuclear Production Facility (a type of ope
Nuclear Plant Supervisor
Nuclear Regulatory Commission
NRC Office of Nuclear Reactor Regulation
Nuclear Regulatory
(NRC Headquarters
Publi
Nuclear Watch Engineer
Outside Lifting System
Operating
Procedure
Original Steam Generator
NRC Public Document
Room
Pressure
Indicator/Controller
Plant Management Action Item
Procedure Qualification Records
Plant St. Lucie
Plant Work Order
Quality Control
RCB
RII
SBCS
St.
TS
UGS
48
Quality Instruction
Reactor Auxiliary Building
'adiation
Control Area
Reactor
Containment Building
Refueling Outage
Region II - Atlanta, Georgia
(NRC)
Radiation Protection
Reactor
Pressure
Vessel
Replacement
Radiation
Work Permit
Steam
Bypass Control System
Steam Generator
Replacement
Project
Steam Generating
Team,
Ltd
Saint
Thermoluminescent
Dosimeter
Technical Specification(s)
Updated Final Safety Analysis Report
Upper Guide Structure
United States
Nuclear Regulatory
Commission
Very High Radiation Area
Violation (of NRC requirements)
Work Order
Work Package
Welding Procedure Specification
Enclosure
2