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Category:CORRESPONDENCE-LETTERS
MONTHYEARML17241A5001999-10-21021 October 1999 Forwards Rev 3 to Emergency Response Data Sys (ERDS) Data Point Library for St Lucie Unit 1.Rev Provides Replacement Pages & Follows Format Recommended by NUREG 1394, ERDS Implementation, Rev 1,App C ML17309A9981999-10-19019 October 1999 Forwards Revised Epips,Including Rev 3 to EPIP-10 & Rev 25 to HP-202.EPIP-10 Added Onsite Monitoring Points,Made Administrative Changes & Incorporated New Attachments & HP-202 Added Red Team Survey Points ML20217F6171999-10-0808 October 1999 Forwards Insp Repts 50-335/99-11 & 50-389/99-11 on 990827 & 990907-09.No Violations Identified.Matl Encl Contained Safeguards Info as Defined by 10CFR73.21 & Disclosed to Unauthorized Individuals Prohibited by Section 147 of AEA ML17241A4811999-10-0101 October 1999 Reports Number of Tubes Plugged During Unit 1 Refueling Outage SL1-16,per TS 4.4.5.5.a ML20212M1601999-09-28028 September 1999 Refers to 990908 Engineering Meeting Conducted at NRC Region II to Discuss Engineering Issues at Lucie & Turkey Point Facilities.List of Attendees & Copy of Presentation Handout Encl ML17241A4701999-09-25025 September 1999 Forwards Info Requested by NRC Staff During 990916 Telcon to Complete Staff Review of Request for risk-informed Extension of Action Completion/Aot Specified for Inoperable Train of LPSI Sys at Plant ML17241A4721999-09-24024 September 1999 Forwards Rev 1 to Plant Change/Mod (PCM) 99016 to St Lucie Unit 1,Cycle 16 COLR, IAW TS 6.9.1.11.d.Refueling Overhaul Activities Are Currently in Progress & Reactor Operations for Cycle 16 Are Scheduled to Commence in Oct 1999 ML17241A4681999-09-22022 September 1999 Requests Restriction Be Added to Senior Operator License SOP-21093 for TE Bolander.Nrc Forms 369,encl.Encl Withheld Per 10CFR2.790(a)(6) ML17241A4671999-09-20020 September 1999 Forwards Completed NRC Form 536, Operator Licensing Exam Data, for St Lucie Units 1 & 2,as Requested in Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing Exams. ML17241A4581999-09-13013 September 1999 Forwards Info Requested by NRC Staff During 990630 & 0816 Telcons,To Complete Review of Proposed License Amend for Fuel Reload Process Improvement Program ML17241A4531999-08-31031 August 1999 Informs That No Candidates from St Lucie Plant Will Be Participating in PWR Gfes Being Administered on 991006 ML17241A4521999-08-31031 August 1999 Withdraws Relief Request 16 & Suppl Relief Request 15 with Info Requested During 990526 Telephone Conference Re ISI Insp Plan,Third 10-yr Interval ML17241A4501999-08-26026 August 1999 Informs That FPL Has Reviewed Reactor Vessel Integrity Database,Called RVID2,re Closure of GL 92-01,rev 1,suppl 1. Requested Corrections & Marked Up Pages from Rvid 2 Database Summary Repts That Correspond to Comments,Attached ML17241A4371999-08-13013 August 1999 Forwards fitness-for-duty Program Performance Data for six- Month Period Ending 990630,per 10CFR26.71(d) ML17241A4461999-08-11011 August 1999 Requests That W Rept Entitled, Evaluation of Turbine Missile Ejection Probability Resulting from Extending Test Interval of Interceptor & Reheat Stop Valves at St Lucie Units 1 & 2, Be Withheld from Public Disclosure L-99-171, Forwards Rev 56 to Physical Security Plan.Summary of Changes & Marked Up Copy of Revised Pages Also Encl.Encls Withheld from Public Disclosure Per 10CFR2.790(a)(3)1999-07-29029 July 1999 Forwards Rev 56 to Physical Security Plan.Summary of Changes & Marked Up Copy of Revised Pages Also Encl.Encls Withheld from Public Disclosure Per 10CFR2.790(a)(3) ML17309A9911999-07-26026 July 1999 Forwards Revised EPIPs & Revised Procedures That Implement Emergency Plan as Listed.Procedures Provides Instruction for Operational Support Ctr (OSC) Chemistry Supervisor to Establish Remote Labs at Locations Specified ML17241A4471999-07-22022 July 1999 Requests That Rev 1 to WCAP-14732 & Rev 1,Add 1 to WCAP-14732 Be Withheld from Public Disclosure ML17241A4221999-07-22022 July 1999 Forwards List of Proposed Licensing Actions for St Lucie Units 1 & 2,planned During Fys 2000 & 2001,in Response to Administrative Ltr 99-02, Operating Reactor Licensing Action Estimates. ML17241A4151999-07-22022 July 1999 Forwards Revised Relief Request 25 for Second 10-yr ISI Interval for Unit 2 ML17241A4101999-07-16016 July 1999 Forwards FP&L Supplemental Response to NRC Request for Info Re Y2K Readiness at Nuclear Power Plants ML17309A9881999-07-0707 July 1999 Forwards Rev 5 to EPIP-03, Emergency Response Organization Notification/Staff Augmentation. Rev 5 to EPIP-03 Was Revised to Transfer EP Responsibilities from Training Manager to Protection Svcs Manager ML20209F1541999-07-0606 July 1999 Informs That NRC in Process of Conducting Operational Safeguards Response Evaluations at Nuclear Power Reactors. Plant Chosen for Such Review Scheduled for Wk of 990823-26 ML17241A4011999-06-30030 June 1999 Forwards Info Copy of Florida Wastewater Permit (FL0002208) (Formerly NPDES Permit) Mod,Which Was Issued by Florida Dept of Environ Protection on 990604 ML17241A3971999-06-30030 June 1999 Forwards Suppl Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs, as Requested in 990317 Ltr ML17355A3661999-06-30030 June 1999 Forwards Florida Power & Light Topical QA Rept, Dtd June 1999.Encl I Includes Summary of Changes Made to Topical QA Rept Since 1998 ML17241A3951999-06-29029 June 1999 Provides Response to NRC Request for Info Re Y2K Readiness at Nuclear Power Plants.Gl 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants, Requested Response on Status of Facility Y2K Readiness by 990701.Disclosure Encl ML17241A3731999-06-17017 June 1999 Supplements Relief Requests 4,11 & 13 for Third ten-year ISI Interval with Info Requested During 990526 Telcon.Expedited Review Is Requested by 990730 to Avoid Negatively Impacting Upcoming St Lucie Unit 1 Refueling Outage (SL1-16) ML17241A3641999-06-14014 June 1999 Submits Supplement to Relief Request 24 with Info Requested by Nrc.In Addition Relief Request 24 Is Identical to St Lucie Unit 1 Relief Request 4 for Third ISI Interval Being Supplemented by FPL Ltr L-99-139 ML20195F3871999-06-11011 June 1999 Final Response to FOIA Request for Documents.App a Records Being Withheld in Entirety (Ref FOIA Exemption 5) IA-99-247, Final Response to FOIA Request for Documents.App a Records Being Withheld in Entirety (Ref FOIA Exemption 5)1999-06-11011 June 1999 Final Response to FOIA Request for Documents.App a Records Being Withheld in Entirety (Ref FOIA Exemption 5) L-99-129, Forwards Rev 55 to Physical Security Plan,Summary of Changes & Marked Up Copy of Revised Pages.With Directions for Incorporating Rev Into Plan & Copies of Replacement Pages.Rev Withheld,Per 10CFR2.790(a)(3)1999-06-0909 June 1999 Forwards Rev 55 to Physical Security Plan,Summary of Changes & Marked Up Copy of Revised Pages.With Directions for Incorporating Rev Into Plan & Copies of Replacement Pages.Rev Withheld,Per 10CFR2.790(a)(3) ML17241A3561999-06-0707 June 1999 Forwards Rept Containing Brief Description & Summary of SEs for Changes,Tests & Experiments Which Were Approved for Unit 3 During Period of 970526-981209 ML17241A3601999-06-0707 June 1999 Forwards Correction to Annual Radiological Environ Operating Rept for CY98.Util Has Identified Transcription Error on Last Page of Attachment C of Rept,Results from Interlaboratory Comparison Program 1998 ML20195F3941999-05-27027 May 1999 FOIA Request That Memo from J Calvo to Fl Lebdon Re TIA - St Lucie,Unit 1 Environ Qualification of Woodward Governor Controls Be Placed in PDR ML17241A3461999-05-24024 May 1999 Forwards Revised Relief Request 22 to Clarify Several Areas of Relief.Nrc Action Is Requested to Be Complete by Aug 1999 to Support Planning for Spring 2000 Unit 2 Refueling Outage ML17241A3391999-05-20020 May 1999 Forwards Notification of Change to Small Break LOCA ECCS Evaluation Model Used for St Lucie Unit 1.Anomaly Was Discovered & Corrected That Resulted in Reducing Calculated PCT for Limiting SBLOCA by More than 50 F ML17241A3371999-05-20020 May 1999 Forwards Util Suppl to GL 95-07 Response Re pressure-locking & Thermal Binding of safety-related power-operated Gate Valves,In Response to NRC Second RAI Dtd 990225 ML20207C7531999-05-17017 May 1999 Discusses Issue Identified by FPL in Feb 1998 Involving Potential for Fire to Cause Breach of Rc Sys High/Low Pressure Interface Boundary & NRC Decision for Exercise of Enforcement Discretion ML17241A3301999-05-17017 May 1999 Forwards LER 99-004-00 Re as Found Cycle 10 Psv Setpoints Outside TS Limits,Which Occurred on 990415.Root Cause Determination Not Yet Complete.Suppl to Include Root Cause & Corrective Actions Will Be Submitted ML17309A9821999-05-10010 May 1999 Forwards Rev 36 to St Lucie Emergency Plan, Per 10CFR50.54(q).Executive Summary & Summary of Changes Incorporated by Rev,Encl IR 05000335/19980141999-04-29029 April 1999 Provides Confirmation of NRC Staff Conclusions Re Cited & non-cited Violations in Insp Rept 50-335/98-14 & 50-389/98-14.Utils Position Re Consideration of Multiple Spurious Actuations in Event of Fire,Reiterated ML17241A3221999-04-29029 April 1999 Provides Confirmation of NRC Staff Conclusions Re Cited & non-cited Violations in Insp Rept 50-335/98-14 & 50-389/98-14.Utils Position Re Consideration of Multiple Spurious Actuations in Event of Fire,Reiterated ML17229B1071999-04-28028 April 1999 Forwards 1998 Annual Environ Operating Rept for St Lucie Unit 2. Rept Includes Discussions of 5-inch Barrier Net Maint & Taprogge Condenser Tube Cleaning Sys Ball Loss,As Agreed at First Biennial Sea Turtle Meeting Held on 980120 ML17229B1051999-04-22022 April 1999 Requests That Listed Individuals Be Placed on Official Serve List for Nuclear Matl Safety & Safeguards Info Notices ML17229B1061999-04-21021 April 1999 Notifies NRC of Change in Medical Status of Licensed Operator Pf Farnsworth (Docket 55-21285,license SOP-21094). NRC Form 3996, Medical Exam Certification, Encl.Encl Withheld Per 10CFR2.790(a)(6) ML17309A9851999-04-15015 April 1999 Requests That NRC Review Denial of Appeal from Assessment of Fees Assessed in 981101 Invoice RS0062-99 & Assessment of Fees in Invoice RS0182-99 Which Was Also Denied in 990305 Ltr.Both Invoices Are for Fees Re Inspector GG Warnick ML20205M0431999-04-13013 April 1999 Eighth Partial Response to FOIA Request for Records.App Q & R Records Encl & Being Made Available in PDR ML17229B0951999-04-0808 April 1999 Requests Approval of Encl Revised Relief Request 6,in Response to 990322 Telcon with NRC & 10CFR55.55a(a)(3). Request States That Visual VT-3 Exams Will Be Conducted IAW IWA-2213 & Repairs Will Be IAW Util ASME Section IX Program ML17229B0821999-04-0707 April 1999 Requests Approval of Interim Relief Request 26 Re Repair Requirements for Class 2 ECCS Piping,Per 10CFR50.55a(a)(3) & 50.55a(g)(iii).Alternative Actions Apply Guidance of GLs 91-18 & 90-05 & ASME Code Case N-513.Evaluation,encl 1999-09-28
[Table view] Category:INCOMING CORRESPONDENCE
MONTHYEARML17241A5001999-10-21021 October 1999 Forwards Rev 3 to Emergency Response Data Sys (ERDS) Data Point Library for St Lucie Unit 1.Rev Provides Replacement Pages & Follows Format Recommended by NUREG 1394, ERDS Implementation, Rev 1,App C ML17309A9981999-10-19019 October 1999 Forwards Revised Epips,Including Rev 3 to EPIP-10 & Rev 25 to HP-202.EPIP-10 Added Onsite Monitoring Points,Made Administrative Changes & Incorporated New Attachments & HP-202 Added Red Team Survey Points ML17241A4811999-10-0101 October 1999 Reports Number of Tubes Plugged During Unit 1 Refueling Outage SL1-16,per TS 4.4.5.5.a ML17241A4701999-09-25025 September 1999 Forwards Info Requested by NRC Staff During 990916 Telcon to Complete Staff Review of Request for risk-informed Extension of Action Completion/Aot Specified for Inoperable Train of LPSI Sys at Plant ML17241A4721999-09-24024 September 1999 Forwards Rev 1 to Plant Change/Mod (PCM) 99016 to St Lucie Unit 1,Cycle 16 COLR, IAW TS 6.9.1.11.d.Refueling Overhaul Activities Are Currently in Progress & Reactor Operations for Cycle 16 Are Scheduled to Commence in Oct 1999 ML17241A4681999-09-22022 September 1999 Requests Restriction Be Added to Senior Operator License SOP-21093 for TE Bolander.Nrc Forms 369,encl.Encl Withheld Per 10CFR2.790(a)(6) ML17241A4671999-09-20020 September 1999 Forwards Completed NRC Form 536, Operator Licensing Exam Data, for St Lucie Units 1 & 2,as Requested in Administrative Ltr 99-03, Preparation & Scheduling of Operator Licensing Exams. ML17241A4581999-09-13013 September 1999 Forwards Info Requested by NRC Staff During 990630 & 0816 Telcons,To Complete Review of Proposed License Amend for Fuel Reload Process Improvement Program ML17241A4531999-08-31031 August 1999 Informs That No Candidates from St Lucie Plant Will Be Participating in PWR Gfes Being Administered on 991006 ML17241A4521999-08-31031 August 1999 Withdraws Relief Request 16 & Suppl Relief Request 15 with Info Requested During 990526 Telephone Conference Re ISI Insp Plan,Third 10-yr Interval ML17241A4501999-08-26026 August 1999 Informs That FPL Has Reviewed Reactor Vessel Integrity Database,Called RVID2,re Closure of GL 92-01,rev 1,suppl 1. Requested Corrections & Marked Up Pages from Rvid 2 Database Summary Repts That Correspond to Comments,Attached ML17241A4371999-08-13013 August 1999 Forwards fitness-for-duty Program Performance Data for six- Month Period Ending 990630,per 10CFR26.71(d) ML17241A4461999-08-11011 August 1999 Requests That W Rept Entitled, Evaluation of Turbine Missile Ejection Probability Resulting from Extending Test Interval of Interceptor & Reheat Stop Valves at St Lucie Units 1 & 2, Be Withheld from Public Disclosure L-99-171, Forwards Rev 56 to Physical Security Plan.Summary of Changes & Marked Up Copy of Revised Pages Also Encl.Encls Withheld from Public Disclosure Per 10CFR2.790(a)(3)1999-07-29029 July 1999 Forwards Rev 56 to Physical Security Plan.Summary of Changes & Marked Up Copy of Revised Pages Also Encl.Encls Withheld from Public Disclosure Per 10CFR2.790(a)(3) ML17309A9911999-07-26026 July 1999 Forwards Revised EPIPs & Revised Procedures That Implement Emergency Plan as Listed.Procedures Provides Instruction for Operational Support Ctr (OSC) Chemistry Supervisor to Establish Remote Labs at Locations Specified ML17241A4221999-07-22022 July 1999 Forwards List of Proposed Licensing Actions for St Lucie Units 1 & 2,planned During Fys 2000 & 2001,in Response to Administrative Ltr 99-02, Operating Reactor Licensing Action Estimates. ML17241A4471999-07-22022 July 1999 Requests That Rev 1 to WCAP-14732 & Rev 1,Add 1 to WCAP-14732 Be Withheld from Public Disclosure ML17241A4151999-07-22022 July 1999 Forwards Revised Relief Request 25 for Second 10-yr ISI Interval for Unit 2 ML17241A4101999-07-16016 July 1999 Forwards FP&L Supplemental Response to NRC Request for Info Re Y2K Readiness at Nuclear Power Plants ML17309A9881999-07-0707 July 1999 Forwards Rev 5 to EPIP-03, Emergency Response Organization Notification/Staff Augmentation. Rev 5 to EPIP-03 Was Revised to Transfer EP Responsibilities from Training Manager to Protection Svcs Manager ML17241A4011999-06-30030 June 1999 Forwards Info Copy of Florida Wastewater Permit (FL0002208) (Formerly NPDES Permit) Mod,Which Was Issued by Florida Dept of Environ Protection on 990604 ML17241A3971999-06-30030 June 1999 Forwards Suppl Response to GL 96-05, Periodic Verification of Design-Basis Capability of Safety-Related Movs, as Requested in 990317 Ltr ML17355A3661999-06-30030 June 1999 Forwards Florida Power & Light Topical QA Rept, Dtd June 1999.Encl I Includes Summary of Changes Made to Topical QA Rept Since 1998 ML17241A3951999-06-29029 June 1999 Provides Response to NRC Request for Info Re Y2K Readiness at Nuclear Power Plants.Gl 98-01, Y2K Readiness of Computer Sys at Nuclear Power Plants, Requested Response on Status of Facility Y2K Readiness by 990701.Disclosure Encl ML17241A3731999-06-17017 June 1999 Supplements Relief Requests 4,11 & 13 for Third ten-year ISI Interval with Info Requested During 990526 Telcon.Expedited Review Is Requested by 990730 to Avoid Negatively Impacting Upcoming St Lucie Unit 1 Refueling Outage (SL1-16) ML17241A3641999-06-14014 June 1999 Submits Supplement to Relief Request 24 with Info Requested by Nrc.In Addition Relief Request 24 Is Identical to St Lucie Unit 1 Relief Request 4 for Third ISI Interval Being Supplemented by FPL Ltr L-99-139 L-99-129, Forwards Rev 55 to Physical Security Plan,Summary of Changes & Marked Up Copy of Revised Pages.With Directions for Incorporating Rev Into Plan & Copies of Replacement Pages.Rev Withheld,Per 10CFR2.790(a)(3)1999-06-0909 June 1999 Forwards Rev 55 to Physical Security Plan,Summary of Changes & Marked Up Copy of Revised Pages.With Directions for Incorporating Rev Into Plan & Copies of Replacement Pages.Rev Withheld,Per 10CFR2.790(a)(3) ML17241A3601999-06-0707 June 1999 Forwards Correction to Annual Radiological Environ Operating Rept for CY98.Util Has Identified Transcription Error on Last Page of Attachment C of Rept,Results from Interlaboratory Comparison Program 1998 ML17241A3561999-06-0707 June 1999 Forwards Rept Containing Brief Description & Summary of SEs for Changes,Tests & Experiments Which Were Approved for Unit 3 During Period of 970526-981209 ML20195F3941999-05-27027 May 1999 FOIA Request That Memo from J Calvo to Fl Lebdon Re TIA - St Lucie,Unit 1 Environ Qualification of Woodward Governor Controls Be Placed in PDR ML17241A3461999-05-24024 May 1999 Forwards Revised Relief Request 22 to Clarify Several Areas of Relief.Nrc Action Is Requested to Be Complete by Aug 1999 to Support Planning for Spring 2000 Unit 2 Refueling Outage ML17241A3371999-05-20020 May 1999 Forwards Util Suppl to GL 95-07 Response Re pressure-locking & Thermal Binding of safety-related power-operated Gate Valves,In Response to NRC Second RAI Dtd 990225 ML17241A3391999-05-20020 May 1999 Forwards Notification of Change to Small Break LOCA ECCS Evaluation Model Used for St Lucie Unit 1.Anomaly Was Discovered & Corrected That Resulted in Reducing Calculated PCT for Limiting SBLOCA by More than 50 F ML17241A3301999-05-17017 May 1999 Forwards LER 99-004-00 Re as Found Cycle 10 Psv Setpoints Outside TS Limits,Which Occurred on 990415.Root Cause Determination Not Yet Complete.Suppl to Include Root Cause & Corrective Actions Will Be Submitted ML17309A9821999-05-10010 May 1999 Forwards Rev 36 to St Lucie Emergency Plan, Per 10CFR50.54(q).Executive Summary & Summary of Changes Incorporated by Rev,Encl ML17241A3221999-04-29029 April 1999 Provides Confirmation of NRC Staff Conclusions Re Cited & non-cited Violations in Insp Rept 50-335/98-14 & 50-389/98-14.Utils Position Re Consideration of Multiple Spurious Actuations in Event of Fire,Reiterated IR 05000335/19980141999-04-29029 April 1999 Provides Confirmation of NRC Staff Conclusions Re Cited & non-cited Violations in Insp Rept 50-335/98-14 & 50-389/98-14.Utils Position Re Consideration of Multiple Spurious Actuations in Event of Fire,Reiterated ML17229B1071999-04-28028 April 1999 Forwards 1998 Annual Environ Operating Rept for St Lucie Unit 2. Rept Includes Discussions of 5-inch Barrier Net Maint & Taprogge Condenser Tube Cleaning Sys Ball Loss,As Agreed at First Biennial Sea Turtle Meeting Held on 980120 ML17229B1051999-04-22022 April 1999 Requests That Listed Individuals Be Placed on Official Serve List for Nuclear Matl Safety & Safeguards Info Notices ML17229B1061999-04-21021 April 1999 Notifies NRC of Change in Medical Status of Licensed Operator Pf Farnsworth (Docket 55-21285,license SOP-21094). NRC Form 3996, Medical Exam Certification, Encl.Encl Withheld Per 10CFR2.790(a)(6) ML17309A9851999-04-15015 April 1999 Requests That NRC Review Denial of Appeal from Assessment of Fees Assessed in 981101 Invoice RS0062-99 & Assessment of Fees in Invoice RS0182-99 Which Was Also Denied in 990305 Ltr.Both Invoices Are for Fees Re Inspector GG Warnick ML17229B0951999-04-0808 April 1999 Requests Approval of Encl Revised Relief Request 6,in Response to 990322 Telcon with NRC & 10CFR55.55a(a)(3). Request States That Visual VT-3 Exams Will Be Conducted IAW IWA-2213 & Repairs Will Be IAW Util ASME Section IX Program ML17229B0821999-04-0707 April 1999 Requests Approval of Interim Relief Request 26 Re Repair Requirements for Class 2 ECCS Piping,Per 10CFR50.55a(a)(3) & 50.55a(g)(iii).Alternative Actions Apply Guidance of GLs 91-18 & 90-05 & ASME Code Case N-513.Evaluation,encl ML17229B0851999-04-0505 April 1999 Requests Approval of Encl Relief Request 25 Which Proposes to Use Alternative Requirements of ASME Code Case N-613 in Lieu of Requirements of ASME Section XI Figures IWB-2500-7(a) & IWB-2500-7(b).Action Requested by Aug 1999 ML17309A9791999-03-31031 March 1999 Forwards Revised EPIPs Including Rev 2 to EPIP-00,rev 2 to EPIP-09,rev 2 to EPIP-10 & Rev 10 to HP-207.Summary of Revs Listed ML17309A9761999-03-23023 March 1999 Forwards Revised Epips,Including Rev 4 to EPIP-03, Er Organization Notification/Staff Augmentation, Rev 3 to EPIP-05, Activation & Operation of OSC & Rev 14 to HP-200, HP Emergency Organization. Changes to Epips,Discussed ML17229B0691999-03-19019 March 1999 Transmits TS Pages Requested by NRC for Use in Issuance of Proposed License Amend Re SFP Storage Capacity,Per Soluble Boron Credit ML17229B0721999-03-16016 March 1999 Requests Approval of Enclosed Relief Requests 23 & 24 Re ISI Plan for Second ten-year Interval.Nrc Action Is Requested to Be Complete by Aug 1999 to Support Planning for Spring 2000 Unit 2 Refueling Outage ML17355A2631999-03-12012 March 1999 Forwards FPL Decommissioning Fund Status Repts for St Lucie, Units 1 & 2 & Turkey Point,Units 3 & 4.Rept for St Lucie, Unit 2 Provides Status of Decommissioning Funds for All Three Owners of That Unit ML17229B0481999-03-10010 March 1999 Informs That Util Delivered Matls Requested in Encl 1 of NRC Ltr by Hand on 990308,as Requested by NRC Ltr Dtd 990218 1999-09-25
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CATEGORY 1
'C ':F REGULR I INFORMATION DISTRIBUTIOhOFSTEM (RIDE)
ACCEPSIION NBR:9610160296 DOC ~ DATE: 96/10/04 NOTARIZED: NO DOCKET N FAC'IL':50-335 St. Lucie Plant, Unit 1, Florida Power & Light Co. 05000335
'AUTH. NAME AUTHOR AFFILIATION STALL,J.A. Florida Power 6 Light Co.
RECIP.NAME RECIPIENT AFFILIATION Document Control Branch (Document Control Desk)
SUBJECT:
Requests approval of Interim Relief Request 20 re containment coolj.ng unit repair,per ISI plan.
DISTRIBUTION CODE: A047D COPIES RECE1VED:LTR ENCL SIZE:
TITLE: OR Submittal: Inservice/Testing/Relief from ASME Code GL- 9-04 NOTES RECIPIENT COPIES RECIPIENT COPIES ID CODE/NAME LTTR ENCL ID CODE/NAME LTTR ENCL PD2-3 LA 1 1 PD2-3 PD 1 1 WIENS,L. 1 1 0 INTERNAL: ACRS 1 1 AEOD/SPD/RAB 1 1 ENTER 1 1 NRR/DE/EMEB 1 1 888~8 RACT 1 1 OGC/HDS3 1 0 RES/DET/EMMEB 1 1 RES/DSIR/EIB 1 1 EXTERNAL: LITCO ANDERSON 1 1 NOAC 1 1 NRC PDR 1 1 D
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NOTE TO ALL "RIDS" RECIPIENTS:
PLEASE HELP US TO REDUCE WASTE. TO HAVE YOUR NAME OR ORGANIZATION REMOVED FROM DISTRIBUTION LISTS OR REDUCE THE NUMBER OF COPIES RECEIVED BY YOU OR YOUR ORGANIZATION, CONTACT THE DOCUMENT CONTROL DESK (DCD) ON EXTENSION 415-2083 TOTAL NUMBER OF COPIES REQUIRED: LTTR 14 ENCL 13
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Florida Power & Light Company, P.O. Box128, Fort Pierce, FL34954-0128 October 4, 1996 L-96-246 10 CFR 50.4 10 CFR 50.55a U. S. Nuclear Regulatory Commission Attn: Document Control Desk Washington, D. C. 20555 RE: St. Lucie Unit 1 Docket No. 50-335 In-Service-Inspection Plan Second Ten-Year Interval Pursuant to 10 CFR 50.55a (a)(3), Florida Power and Light Company (FPL) requests approval of Interim Relief Request 20. The interim relief requested is for the temporary non-code repair of the ASME Class 3 containment cooling unit coil, HVS-1B. FPL has determined pursuant to 10 CFR 50.55a (a)(3) that the proposed alternatives would provide an acceptable level of quality and safety, or that compliance with the specified requirements would result in hardship or unusual difficulty without a compensating increase in the level of quality and safety. Attachment A is Interim Relief Request 20 and Attachment B is the engineering basis for the temporary repair.
Please contact us if there are any questions about this submittal.
Very truly yours, J. A. Stall Vice President St. Lucie Plant JAS/GRM cc: Stewart D. Ebneter, Regional Administrator, Region II, USNRC Senior Resident Inspector, USNRC, St. Lucie Plant 9610160296 96i004 PDR 8
ADOCK 05000335 PDR Ii an FPL Group company
St. Lucie Unit 1 Docket No. 50-335 L-96-246 Attachment A Page A-1 Relief Request No. 20, Containment Cooling Unit Repair A. Component Identification Code Class 3 Containment Cooling Unit HVS-1B B. Code Requirement ASME Section XI, 1983 Edition with Addenda thru Summer 1983 IWD-4000 Repair Procedures requires defects to be removed in accordance with IWD-4200 C. Relief Requested During operation, leakage was detected on containment cooling unit HVS-1B. The leakage was found on a 3" brazed joint of a dissimilar metal weld, carbon steel to copper pipe.
Relief is requested from the repair requirements of the ASME Boiler and Pressure Vessel Code,Section XI, 1983 Edition through the Summer 1983 Addenda, Articles IWA/IWD-4000.
D. Basis for Relief See Attachment B.
E. Alternative Repair FPL will perform a temporary non-code repair on the containment cooling unit as described in the basis for relief.
This temporary repair will perform the function of leakage prevention and will remain in place no later than startup after the next scheduled refueling outage or scheduled outage greater than 30 days in length. At that time, a Code repair/replacement will be performed.
F. Implementation Schedule St. Lucie Unit 1, Cycle 14, until the next refueling outage (SL1-15) or scheduled outage greater than 30 days in length.
G. Attachments to the Relief Engineering basis for performing a temporary non-code repair.
St. Lucie Unit 1 Docket No. 50-335 L-96-246 Attachment B ST ~ LVCIE UNIT 1 FLORIDA POWER & LIGHT COMPANY ENGINEERING JUSTIFICATION TEMPORARY NON-CODE REPAIR RELIEF REQUEST FOR HVS-1B COOLING COIL SUPPLY LINE
St. Lucie Unit 1 Docket No. 50-335 L-96-246 Attachment B Page B-.2 Interim Relief Request'for Containment Cooling Unit HVS-1B Repair During plant operation, on August 26, 1996, a leak was discovered in a brazed joint on one of the six (6) cooling coil banks for the 1B containment cooling unit (HVS-1B). The leak was located in the brazed joint between the 3 inch carbon steel pipe stub and 3 inch copper coil header piping. The leak had been characterized as 6 to 8 separate pin hole leaks in the joint brazing material. The pin hole leaks are in close proximity to one another.
Florida Power and Light Company (FPL) has determined that an ASME Section XI repair, is not practical at this time. In order to perform the necessary Code repair, one of the two containment cooling trains would have to be isolated and taken out of service.
Containment cooling unit HVS-1B would have to be drained and the cooling coil removed to allow for joint disassembly. Complete disassembly of the brazed joint would be required in order to clean and re-braze the joint properly and eliminate the potential for any subsequent leakage. The cooling coil would have to be reinstalled and successfully leak tested prior to placing HVS-1B back in service. Due to the size and weight of the cooling coil, all of the necessary work would have to be performed inside containment while the unit is operating at power. Temperatures inside containment typically average up to 100'F. At this temperature, stay times of up to only 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> are allowed in order to avoid heat stress to plant personnel. Dose rates in the area of HVS-1B have been measured at 50 mR/hr. Performance of a Code repair while the unit is at power would also result in unnecessary personnel exposure. Due to the overall complexity of a Code repair, the Technical Specification allowed outage time (AOT) for the affected containment cooling train of 7 days may also be insufficient. FPL has determined a plant shutdown and cooldown with unnecessary cycling of facility systems and components would then be required to perform a Code repair. The proposed temporary non-Code repair alternative would provide an acceptable level of quality and safety. Compliance with ASME Section XI would result in hardship or unusual difficulty without a compensating increase in the level of quality and safety. A Code repair/replacement will be accomplished during the next scheduled outage exceeding 30 days and no later than the next scheduled St. Lucie Unit 1 refueling outage (SL1-15) which is currently scheduled for the Fall of 1997.
St. Lucie Unit 1 Docket No. 50-335 L-96-246 Attachment B Page B-3 St. Lucie Unit 1 has four (4) containment cooling units located inside containment. The safety related functions of the cooling units is to provide heat removal from the containment air/steam mixture following a loss of coolant accident (LOCA) or main steam line break (MSLB) to prevent the containment building from exceeding its design pressure and temperature limits. The cooling units also provide for circulation of the containment atmosphere post-accident to prevent stratification and formation of hydrogen gas pockets inside containment.
Each cooling unit contains 6 cooling coil banks that are supplied with cooling water from the safety related closed loop component cooling water (CCW) system. The affected portion of the CCW system piping also functions to maintain containment integrity.
The cooling coils and associated CCW system piping for the containment cooling units are classified as Quality Group C (Class 3). In accordance with the guidance specified in NRC Generic Letter 90-05, Guidance for Performing Temporary Non-Code Repair of ASMZ Code Class 2, 2, and 3 Piping, the subject piping is classified as moderate energy (maximum operating temperature less than 200'F and maximum operating pressure less than 275 psig).
Once the operational leakage was discovered, an evaluation was performed which concluded that an operability concern does not exist. Continued monitoring and additional visual inspections of the leakage were performed. Subsequent inspections concluded that the leakage had not worsened.
In accordance with the guidance of Generic Letter 90-05, a leak repair enclosure has been installed as a stopgap measure to eliminate the leakage. Once written relief is granted by the NRC, this leak repair enclosure is intended to function as a temporary non-code repair in the interim period until a Code repair can be accomplished.
As stated above, the subject leak had been characterized as 6 to 8 separate pin hole leaks in the joint brazing material which are in close proximity to one another. The approximate leak rate was initially measured to be 1.5 gallons per hour. Subsequent and more accurate leak rate measurements yielded a leak rate of less than 1 gallon per hour. The flaws were initially characterized by visual inspection. While performing the visual inspections, determined that additional volumetric examinations were not it was feasible based on the joint geometry and the copper pipe to carbon
St. Lucie Unit. 1 Docket No. 50-335 L-96-246 Attachment B Page B-4 steel pipe stub brazed joint construction. The visual inspections have provided sufficient information to characterize the flaws without the use of additional volumetric examinations.
A similar pin hole leak was discovered in essentially the same location during the recent St. Lucie Unit 1 refueling outage.
Brazing of the joint was performed during the refueling outage and the leak was initially eliminated. However, subsequent inspections performed during plant operation identified additional pin hole leaks in the repaired area. The failure mechanism has been determined to most likely be the propagation of subsurface defects in the brazed joint filler material. Brazing defects can include flux inclusions, lack of adhesion or porosity. A subsurface defect likely propagated through the repair brazing filler material resulting in the subject leak.
Based on the location and size of the current and past'eaks and postulated causative failure mechanisms, current flaws will propagate significantly it in is unlikely that the the near term. Rapid propagation of the defects as a result of external loads is not expected based on the restrained configuration of the associated piping system. Flaw propagation due to overload is unlikely since joint loading conditions are not expected to change significantly during plant operation.
The flaw evaluation methodology contained in NRC Generic Letter 90-05 is not applicable since the flaws are located in the brazed joint filler material and are not believed to be flaws through the copper or steel piping base material. In addition, volumetric examinations are not considered feasible based on the joint geometry and the copper pipe to carbon steel pipe stub brazed joint construction.
Additional walkdowns/inspections of the leak have been performed since initial discovery. The results of the inspections concluded that additional flaw propagation had not occurred and the leak had not worsened. In accordance with the guidance of NRC Generic Letter 90-05 for Class 3 moderate energy piping, a leak repair enclosure has been installed as a stopgap measure to eliminate the leakage while preparing this relief . request. Subsequent inspections have indicated that the stopgap leak repair enclosure has been successful in eliminating the leakage.
The interim method for, eliminating the subject leakage is the installation of an engineered leak repair enclosure. The enclosure has been designed for the maximum internal and external design
St. Lucie Unit 1 Docket No. 50-335 L-96-246 Attachment B Page B-5 pressure and temperature conditions. The enclosure is constructed of standard carbon steel plate material and alloy bolting. The enclosure has been designed to encapsulate both the copper header piping and the carbon steel pipe stub. This design assures that the entire brazed joint is contained within the enclosure.
Injection compound approved for use in the subject application is utilized as a supplemental sealing mechanism-.
The installation of the leak repair enclosure has been evaluated for potential impact on the structural integrity of the affected components/piping system. The additional loads (dead weight and seismic) imposed by the leak repair enclosure are acceptable and has been concluded that the structural integrity of the existing it components/piping system is unaffected.
The proposed non-Code repair will remain in place until a permanent ASME Section XI Code repair/replacement is performed. In accordance with the guidance of NRC Generic Letter 90-05, the Code repair/replacement will be completed no later than the next scheduled Unit 1 outage exceeding 30 days or during the next scheduled refueling outage.
As required by NRC Generic letter 90-05, fifteen (15) additional potentially susceptible locations were visually inspected for signs of leakage. The inspections were limited to the CCW supply piping connections to the cooling coils on containment cooling units HVS-1A, 1B and 1D. No leakage was identified from these additional locations. Also in accordance with the guidance of NRC Generic Letter 90-05, the structural integrity of the proposed temporary non-Code repair will be assessed periodically during the normally scheduled containment anomaly inspection. The containment anomaly inspections are typically performed once every two weeks.
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