ML17229A032

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Insp Repts 50-335/96-11 & 50-389/96-11 on 960707-0803. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support
ML17229A032
Person / Time
Site: Saint Lucie  NextEra Energy icon.png
Issue date: 08/31/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML17229A030 List:
References
50-335-96-11, 50-389-96-11, NUDOCS 9609170377
Download: ML17229A032 (34)


See also: IR 05000335/1996011

Text

i

U.S.

NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos:

50-335,

50-389

License

Nos:

DPR-67,

NPF-16

Report

No:

50-335/96-11,

50-389/96-11

Licensee:

Florida Power

5 Light Co.

Facility:

St. Lucie Nuclear Plant,

Units

1

5 2

Location:

9250 West Flagler Street

Miami,

FL 33102

Dates:

July

7 - August 3,

1996

Inspectors:

M. Miller, Senior Resident

Inspector

J.

Munday, Resident

Inspector

P. Fillion, Reactor Inspector,

paragraph

E2.2

W. Bearden,

Reactor Inspector,

paragraph

M2.3

J. York, Reactor Inspector,

paragraph

El. 1

Approved by: K. Landis, Chief, Reactor

Projects

Branch

3

Division of Reactor Projects

9609i70377 96083i

PDR

ADOCK 05000335

6

EXECUTIVE SUMMARY

St.

Lucie Nuclear Plant, Units

1

8

2

NRC Inspection

Report 50-335/96-11,

50-389/96-11

This integrated

inspection

included aspects

of licensee

operations,

engineer-

ing, maintenance,

and plant support.

The report covers

a four week period of

resident

inspection.

~0erati ons

~

Unit

1 entered

reduced

inventory conditions

on July 9 and July 11.

Operations

exerted

appropriate controls during the evolutions.

Management

involvement in incorporating the movements of Hurricane

Bertha into the reduced

inventory plans

was noteworthy.

Reduced

inventory control continues to be

an operational

strength

at St. Lucie

(paragraph

01.2).

~

The licensee

was proactive

and responsible

in preparing for potential

impact from Hurricane Bertha

(paragraph

01.3).

~

An overspeed trip of the

2C Auxiliary Feedwater

Pump occurred during the

period

as

a result of operator error (paragraph

02. 1).

~

An event involving the isolation of charging

and letdown,

and

a minor

water

hammer event,

occurred.

The licensee's

root cause activities were

followed and were not complete at the

end of the inspection

period

(paragraph

02.2).

~

A gA audit was reviewed

and found to be thorough.

gA-identified

administrative errors resulted

in a non-cited violation (paragraph

07.1).

Maintenance

A review of Control

Element Assembly maintenance

indicated that the

licensee's

preventive maintenance

program

was adequate.

An increase

in

the amount of predictive maintenance

was found to have contributed to

a

reduction in the

number of rod drop events

(paragraph

M2.3).

A Unit 2 charging

pump discharge

check valve stuck open during the

period, resulting in a bypass

flowpath from the charging

pumps to the

volume control tank and the declaration of a Notification of Unusual

Event.

The licensee's

root cause

determination

and corrective action

were reviewed

and found to be acceptable

(paragraph

M2. 1).

A walkdown of the Unit

1 containment building at normal operating

temperature

and pressure

(prior to the Unit

1 startup

from a refueling

outage)

was performed.

Post-outage

cleanliness

was found to be

excellent

(paragraph

M2.2).

A review of freeze seals

applied during the Unit

1 outage identified one

instance

in which a freeze

seal

had

been left unattended

while an area

cleanup

was performed, resulting in a non-cited violation (paragraph

H3.1) .

En ineerin

An issue involving the prelubrication of valves prior to surveillance

testing,

which was identified in 1995,

was resolved.

The practice,

which had

been explicitly required in a procedure,

was found to be in

violation of the

Code of Federal

Regulations

(paragraph

E2. 1).

A review of engineering activities surrounding control element

assembly

reliability was conducted

and found to be satisfactory

(paragraph

E2.3).

Auxiliary Feedwater Actuation System setpoints

were found to be

nonconservative

due to an apparent failure to incorporate as-built

dimensiors

in a calibration calculation.

The issue

was designated

an

Unresolved

Item pending conclusion of the licensee's

root cause

investigation

(paragraph

E2.3).

The licensee

entered

Technical Specification 3.0.3

due to the miswiring

of three channels of linear nuclear instrumentation

during the Unit

1

outage.

The miswiring error involved reversing

inputs from the upper

and lower detectors for the three channels,

which adversely affected

axial

shape

index values.

The issue will be tracked

as

an Unresolved

Item pending completion of inspection activities for this event

(paragraph

E2.4)

The licensee's

engineering

and the

gA organizations

performed thorough

inspections

and assessments

of the tube plugging process

that resulted

in a finding, recommendations,

and concerns.

Resolution of the issues

was satisfactory

(paragraph

E2.4).

Re ort Oetails

Summar

of Pl-nt Status

Unit

1 entered

the inspection period in Node

5 during

a refueling outage.

The

unit was taken critical on July 23 and entered

Node

1 on July 25.

Full power

conditions were achieved

on July. 29.

Unit 2 entered

the inspection period at full power and operated

at essentially

full power throughout.

I. 0 erations

01

Conduct of Operations

Ol. 1

General

Comments

71707

Using Inspection

Procedure

71707,

the inspectors

conducted

frequent

reviews of ongoing plant operations.

In general,

the conduct of opera-

tions

was professional

and safety-conscious;

specific events

and

noteworthy observations

are detailed

in the sections

below.

01.2

Reduced

Inventor

0 erations

71707

a ~

b.

Scope

On July 9, at 3:30 a.m., Unit

1 entered

reduced

inventory to inspect for

the existence of a tube plug in

SG

1B (reviews

had indicated that this

plug may have

been left out following in-situ pressure testing).

The

RCS level

was restored

to normal level at ll:16 on July 10.

While the

RCS was at

a reduced

inventory,

a number of controls

and procedures

were

implemented to ensure

the safety of the unit.

Two procedures

implemented

were:

AP 0010145,

Rev 10,

"Shutdown Cooling Controls"

and

AP

1-0410022,

Rev 27,

"Shutdown Cooling", Appendix A, "Instructions for

Operations

at Reduced

Inventory or Mid-loop Conditions."

Findings

The inspector

reviewed the following items during this evolution:

~

Containment

Closure Capability - The equipment

hatch

was closed

during the evolution.

The inspector

reviewed the penetrations

which remained

open

and verified that closure capability was

available.

~

RCS Temperature

Indication - Two

SPDS channels,

containing

multiple CET indications,

were available.

~

RCS Level Indication - Independent

RCS wide and narrow range level

instruments,

which indicated in the control

room, were operable.

An additional

Tygon tube loop level indicator was installed in the

containment

and

was visible to a dedicated

operator in the control

room via

a television monitor.

~

RCS Level Perturbations

- When

RCS level reduction

was initiated,

additional operational

controls were invoked.

Plant staff were

advised of the reduction in

RCS level

and Operations

took action

to ensure that maintenance

would not perform work that might

effect

RCS level or shut

down cooling.

~

RCS Inventory Volume Addition Capability - One

HPSI

pump

and

one

charging

pump were available for inventory addition,

as were two

trains of shutdown cooling.

~

RCS Nozzle

Dams - The

RCS nozzle

dams

were not installed at the

time.

~

Vital Electrical

Bus Availability - Operations

did not release

busses

or alternate

power sources for work while the unit was in a

reduced

inventory.

Both

EDGs were available.

~

Pressurizer

Vent Path

- The manway atop the pressurizer

was

removed to provide

a vent path

and Operations verified that the

manway

was unobstructed

'every four hours.

Given the fact that Hurricane Bertha

was moving through the Carribean

during the evolution, the licensee's

evaluations prior to initiating

reduced

inventory evolutions involved basing actions

times

on projected

hurricane landfall predictions.

Schedules

prepared for the evolution

allowed for approximately

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of margin between

the time projected

for exiting reduced

inventory conditions

and worst-case

projected

landfall.

The inspector considered

the licensee's

scheduling for this

evolution to show good safety consciousness.

The Unit was again taken to reduced

inventory conditions

on July ll,

after it was clear that Hurricane Bertha

was not going to affect the

local area.

The purpose of this evolution was to inspect

two tubes in

the lA SG for the existence of tube stabilizers

which post-outage

reviews indicated

had

been left out following outage work.

The

inspector verified that the items

above

remained

in affect for this

second evolution.

Reduced

inventory conditions

were exited

on July 12.

Conclusions

Operations

exerted appropriate

controls while the

RCS was in reduced

inventory.

Hanagement

involvement in establishing

schedules

which

properly factored Hurricane Bertha into the initiation of reduced

inventory activities

showed

good safety consciousness.

Reduced

inventory controls continue to be

an Operations

strength at St. Lucie.

01.3

a 0

b.

C.

Hurricane Preparations

(71707)

Scope

During the week of July 8 through

12, Hurricane Bertha

was moving

through the Carribean with projected point of landfall ranging,

alternatively,

from southern to northern Florida.

During the period,

the inspectors'followed

the licensee's

preparations

for the storm.

Findings

While National

Weather Service projections

placed

low probabilities of

landfall near the site,

the licensee

began to perform selected

portions

of AP 0005753,

revision

18,

"Severe

Weather Preparations,"

throughout

the week.

Host activities involved long lead time evolutions

such

as

filling storage

tanks,

removing loose material

from outside

areas,

and

organizing storm crews.

By July 10, the licensee

had designated

personnel

to report to the site

at 8:00 p.m. that night and to remain through the storm.

The inspectors

performed

a walkdown of external

plant areas

and found conditions

generally satisfactory.

As conditions never actually materialized

which

would require entry into the subject

procedure

(Hurricane

Watch or

Hurricane Warning), the inspectors

found that the licensee

had

been

conservative

and

had exercised

good judgement in preparing early.

Conclusion

02

02.1

The inspectors

concluded that the licensee

had acted responsibly

and

conservatively

in the actions

taken to prepare

the plant for the

potential

impact from Hurricane Bertha.

Operational

Status of Facilities

and Equipment

2C Auxi1i ar

Feedwater

Pum

Overs

eed

71707

92902

'a ~

Scope

On July 16, the

2C Auxiliary Feedwater

Pump tripped

on electrical

overspeed

following PM activities.

The system

had

been placed

under

clearance

to perform the

PM activities.

The clearance

isolated

the

turbine trip and throttle valve,

however the warmup bypass

valves were

left open.

This allowed

a short section of piping to pressurize

with

steam.

When the clearance

was lifted and 'the trip and throttle valve

was reopened

the residual

steam in the piping caused

the turbine to

increase

speed until it was exhausted

at which time it coasted to a

stop.

It was then restarted

and subsequently

tripped

on electrical

overspeed.

The inspector followed the licensee's

activities with regard

to. this event.

,

C.

Findings

The licensee initiated an In-House

Event Report

and preliminarily

concluded that the turbine was not allowed to remain idle

a sufficient

amount of time following the turbine roll when the clearance

was lifted.

A Condition Report

was initiated but had not been finalized at the

conclusion of this reporting period.

OP 2-070050 stated that

a minimum of three minutes

between turbine runs

was required to prevent

overspeed.

The reason for the idle time was to

allow entrapped

governor control oil to bleed out from under the main

speed piston within the Woodward governor.

Failure to observe

the three

minute period could cause

the turbine to overshoot to the overspeed trip

setpoint during

a subsequent

startup.

An alternate

method to bleed the oil was to lower the governor

speed

control

knob to its lowest

speed setting,

which would rapidly dump the

oil to its

own sump.

The inspector reviewed the procedure

being

used to

operate

the system

when the trip occurred,

OP 2-00700050,

revision 42,

"Auxiliary Feedwater

Periodic Test,"

and concluded that adequate

guidance

was provided to prevent tr'ipping the turbine because

of this

condition.

In addition, the inspector

reviewed the licensee's

Offnormal

and

Emergency

Operating

procedures

and verified that adequate

guidance

existed for correcting this condition should the turbine trip and

need

to be immediately restarted.

The inspector questioned

the licensee

about system operability during

the period of time it takes the oil to drain back to the

sump.

The

concern

was that although the period of inoperability was short, if

another Technical Specification

(TS) required

system

was also

inoperable,

another

TS action statement

might apply and

go unnoticed.

The Operations

Manager agreed

and stated that the turbine driven

AFW

pumps would be logged out of service following future periods of

operation.

Conclusion

The inspector

concluded that the licensee

had appropriately

addressed

this issue.

02.2

Unit

1 Char in

Letdown Issues

71707

a ~

Scope

On July 20, Unit

1 was in Mode

3 and work was being performed

by IKC to

adjust temperature

alarm setpoint for TIA-1111X and TIA-1121X to new

values

as

a result of higher expected

values of hot leg temperature

due

to increased

levels of SG tube plugging which took place during the Unit

1 refueling outage.

During the calibration,

I&C lifted leads

on TE-

1121X to place

a resistance

decade

box across

the temperature

indication

circuitry.

The act of lifting the leads

created infinite resistance

from the subject

RTD, resulting in a maximum indicated temperature.

Unknown to

IKC at the time was the fact that the

RTD in question

was

providing

a temperature

input to

RRS channel

2, which employed the

temperature

input to develop

a programmed pressurizer

level.

With

maximum temperature

input to

RRS 2,

programmed pressurizer

level rose to

a full-power-equivalent

(66%) value.

Operators

noted the increase

and

directed

IKC to restore

the channel

to normal.

During this action,

the

two operating

charging

pumps

(8 and

C) stopped

operating.

Operators

secured

letdown

as

a result of the secured

charging

pumps.

The

inspector followed the licensee's

actions

in response

to this event.

Findings

CR 96-1792

was initiated following the event.

The inspector discussed

the issue of charging

pump operation with the engineers

assigned

to the

project.

The engineers

found that the charging

pumps

had stopped

operating

due to selector

switch misalignment

on the control panel.

The unit had three charging

pumps.

Normally one

pump was in operation

and the second

and third pumps were preselected

by selector switch for

backup operation.

By design, if pressurizer

level fell below -3% of

programmed level, the first backup

pump would start

(when level

was

restored

to

-1% of programmed level, the

pump would stop).

If level

continued to drop, the second

backup

pump would start

when pressurizer

level fell below

-4% of programmed level

(when level

was restored

to

-2%

of programmed level the

pump would stop).

Prior to the event,

the licensee

was operating the IB and

IC charging

pumps,

and the backup

pump selector

switch was selected

such that these

two pumps were designated

as backups.

When I&C's actions resulted

in an

increase

in pressurizer

level program,

the

pumps continued to run in a

backup

mode.

When program level returned to normal

(matching

approximately actual level) the two pumps stopped,

as would be expected

by design.

The inspector reviewed the appropriate

CWDs with the

licensee's

engineer

and concurred with this conclusion.

Following the event,

operators

attempted to restore

charging

and letdown

to service.

Upon initiating letdown,

a loud noise

was heard

by

personnel

in the area

on the regenerative

heat exchanger

in containment

and operators

noted that letdown automatically isolated.

Concurrently,

a regenerative

heat exchanger

high differential pressure

alarm was

received in the control

room.

The system design

included

an automatic

letdown isolation under

such conditions.

The licensee

concluded that

a

probable

waterhammer

event

had occurred

when letdown was restored.

The

licensee

performed

an engineering

walkdown of piping associated

with the

regenerative

heat exchanger

and determined that

no damage

had occurred.

An engineering

evaluation

was

commenced

to--determine

the susceptibility

of the system to such

an event.

At the close of the inspection period,

the evaluation

was not complete.

At. the end of the inspection period,

the subject

CR was still open.

The

adequacy of the licensee's

overall investigation will be reviewed

upon

closure of the

CR.

Accordingly, this will be tracked

as

an inspector

C.

follwup item (IFI 50-335/96-11-01,

"Adequacy of Root Cause

Investigation

for Unit

1 Charging

System Anomalies" ).

Conclusion

07

07.1

The inspector

concluded that the licensee's

determination of root cause

for observed

charging

pump performance

was satisfactory.

Issues

relating to the overall evaluation of the event will be covered in

subsequent

inspections.

equality Assur ance in Operations

A Audit Re ort Concernin

The

STAR PMAI Conversion

Process

40500

a

~

b.

Scope

In April, the Condition Report

(CR) process

superseded

the existing St.

Lucie Action Request

(STAR) process for documenting

adverse

conditions.

The licensee's

goal

was to have

a uniform Nuclear Division Condition

Report process

to document,

evaluate,

track,

and correct conditions of

concern to site personnel.

During the period of transition from STARs

to

CRs the licensee

used the newly developed

Plant Manager's

Action Item

(PMAI) tracking system to document

any outstanding

actions

associated

with STARs.

This tracking system

was

implemented

in January

and

was

designed

to track action items

on

a plant wide basis.

During this

inspection period,

the inspector

reviewed

gA audit report 96-05,

which

evaluated this conversion

process.

Findings

In general,

the audit found that

STARs whose actions

had

been

completed

were simply closed.

For STARs containing outstanding

actions,

PMAI's

were initiated to track those actions

and then the

STAR was closed.

The

audit identified three findings.

The first finding stated that the

PMAI

procedure

lacked

adequate

guidance

and

was

implemented without first

providing training for the affected personnel.

The licensee

stated that

the procedure

was being successfully

used at Turkey Point and

was simply

implemented without considering

the impact it would have

on personnel

at

St. Lucie who had

no working knowledge of the process.

The inspector

reviewed

AP 0006129, revision

1,

"PMAI Corrective Action Tracking

Program,"

and noted that,

since the finding, the procedure

had

been

revised to clarify points of confusion.

The second finding identified that the Corrective Actions department

was

closing

STARs without first receiving concurrence

from the initiating

department

when required.

The Corrective Actions department

head

admitted that this had occurred

but stated that

an independent

review

was substituted for the originator's concurrence,

which was the method

used

by the

new

CR process.

He stated that

he

had submitted

a procedure

revision requesting that this requirement

be deleted.

However, the

procedure revision

was not approved

by gA and the Corrective Actions

group

was not made

aware that the revision

had

been denied.

As a

result,

the originator's concurrence

was not obtained in all cases

as

required

by 91 16-PR/PSL-2,

Rev.

4, "St. Lucie Action Report

(STAR)

Program,"

step 5.6. 1.B.

The licensee's

corrective action included

discussing

procedural

compliance

requirements

with the involved

individuals.

In addition, the Corrective Action group

has

been put on

distribution for the procedures

they normally use.

The inspector

concluded that the licensee's

failure to obtain the originator's

signature constituted

a violation of the licensee's

procedure.

However,

the inspector

noted that the issue

was administrative

in error,

appeared

to be limited in scope

and impact,

and did not impact the actual

disposition of the issues

described

in the affected

STARs.

Therefore,

this licensee identified and corrected violation is being treated

as

a

Non-Cited Violation, consistent

with Section VII.B.1 of the

NRC

Enforcement

Policy

(NCV 335,389/96-11-02,

"Failure to Obtain

Originator's

Concurrence

During STAR Closeout" ).

The inspector

reviewed approximately seventy-five

STARs which had

been

converted to the

CR/PHAI process

and noted the

same deficiency

identified by gA.

In addition, the inspector

noted several

STARs for

which final approval

by the Plant General

Manager

(PGM) was provided

by

someone

other than the

PGM.

STARs 960355,

940428,

and

960459 were

identified as requiring

PGH approval prior to being closed;

however,

the

PGH blank was signed

by a member of the Corrective Actions group not

having

PGM signature authority.

The

STARs were closed with the

outstanding

actions

being transferred

to the

PMAI process.

In addition

the inspector

noted that the majority of the

STARs which didn't require

PGH concurrence

had

been

signed

by someone without his authority.

The

Corrective Actions group

head stated that this was not an attempt to

circumvent

PGM concurrence,

but rather to simply transfer documentation

and closeout to the

new process.

It would appear that the unauthorized

signatures

were simply a result of closing out

a large quantity of

documents

over

a short period of time.

Although not

a violation of

procedural

requirements

the inspectors felt this action

was not prudent.

This issue

was discussed

with the

PGH who stated that it did not meet

his expectations

either.

He stated that

he would discuss this with the

personnel

involved.

The inspectors

considered this course .of action to

be appropriate.

The third finding noted that near term corrective actions

associated

with three

STARs had the due dates

extended

when converted to PHAIs.

The issues

surrounding

the three

STARs were evaluated

and dispositioned

upon identification.

Additionally, in response

to this finding, the

affected

group reviewed approximately

20% of the nonconforming

STARs for

closeout

adequacy

and found no discrepancies.

Conclusion

The inspector

concluded that the

gA audit was thorough

and contained

findings of substance.

The responses

to the findings by the affected

organizations

adequately

addressed

the concerns.

One poor practice with

regard to the delegation of signature authority was identified.

II. Haintenance

maintenance

and Material Condition of Facilities

and Equipment

2C Char in

Pum

Dischar

e Check Valve Failure

62703

93702

71750

Scope

On July 13, while swapping charging

pumps to perform maintenance,

control

room operators

received

annunciator

N-14, charging

pumps flow

low, and

upon observing charging flow decrease

to 0 gpm, isolated the

charging

and letdown flow paths.

The inspector followed the licensee's

activities in response

to this event.

Findings

Prior to this occurring the

2C charging

pump had

been

placed in service

so that the

2B pump could

be secured for lube oil addition.

Upon

completion of this activity, the

2B pump was restarted

and the

2C

pump

was secured.

It was at that time that the low pump flow annunciator

alarmed

and the operator

observed

flow to be decreasing.

In an attempt

to recover flow, the operator started

the

2A charging

pump,

however

as

the flow continued to decrease

the operator isolated the charging

and

letdown flowpaths

and requested

the

SNPO investigate.

Initial reports

indicated

a considerable

leak coming from the

2B charging

pump packing.

The

pump was isolated

and the leak subsided.

The

2C charging

pump was

placed

back in service

and normal charging

and letdown operation

was

restored.

Because

the charging flow had decreased

to 0 gpm with two

pumps in service,

the licensee

assumed

the cause

was

due to the

2B pump

packing leak

and subsequently

declared

an Unusual

Event in accordance

with plant procedures.

In addition,

a one hour emergency notification

was

made to the

NRC in accordance

with 10 CFR 50.72(a)(1)(i).

Subsequent

investigation determined that the packing leak was not as

large

as originally thought

and

was not the cause of the loss of flow.

The licensee

concluded that

when the

2C pump was secured

the discharge

check valve,

V2167, stuck open.

Because

the

pump recirculation valve,

which is located

upstream of the check valve,

opens

when the

pump is

secured,

a flow path

was established

from the

2B pump backwards

through

the stuck open check valve

and recirculation valve for the

2C pump to

the volume control tank.

An engineering

evaluation

was performed to

determine

the approximate

packing leakage rate

and

a value of 4. 1

gpm

was calculated.

On August 1, the licensee retracted

the

one hour

notification.

The licensee initiated work order 96018092 to disassemble

and replace

the valve disc which the inspector witnessed

on July 17.

When the valve

bonnet

was removed,

the disc was observed to be stuck open approximately

one-half inch.

After the disc was removed,

the internal

bore

was noted

to. have

a casting void between

the discharge

port and the top of the

valve bore approximately

1 - 1.5 inches wide.

The bore normally

measured

1.879 inches to 1.881

inches,

however,

in this void area the

bore was 1.887 inches.

A second

valve from the warehouse

was

disassembled

on July

18 and

was observed

to contain machining marks

on

the circumference of the valve bore in the

same location.

The licensee

subsequently

disassembled

a total of 35 check valves from the warehouse

and noted machining/casting

flaws in 23.

In each valve inspected,

the bore

had

a rough surface

adjacent to the

outlet port of the valve spanning

an arc of approximately

60 degrees.

Although the cause of the roughness

was not conclusively determined it

appeared

to be

a result of the manufacturing

process.

Possible

causes

included mis-registration of the piston bore core during casting of the

valve body blank, mis-positioning of the blank, or mis-positioning of

the fixture used to hold the casting blank during machining.

These

valves were two inch stainless

steel

Anchor Darling piston check valves.

The findings were documented

in the

CR 96-1774.

Following discussions

between

the license,

Anchor Darling,

and the

NRC, Anchor Darling

submitted

a letter to the

NRC stating that

a potential

10 CFR Part 21

condition existed

and stated that the concern

would be shared with their

customers.

The licensee identified other systems

in the plant where this model

valve was located

and assessed

each application for operability.

The

valves were located in the HPSI,

AFW and

IA systems

on Unit

1 and the

CS,

LPSI,

HPSI,

IA, and

SA systems

on Unit 2.

The operability

assessments

were reviewed

and approved

by the Facility Review Group

(FRG).

A maintenance

schedule

was also developed for inspection

and

repair.

The inspectors

reviewed the licensee's

assessment

and after

conferring with the licensee,

Anchor-Darling,

and

NRR concluded that

actions

being taken

by the licensee

were appropriate.

While observing

Maintenance

personnel

disassemble

the V2167, the

inspector noted that the tools

and equipment

needed

to support the job

had

been laid out and arranged

on the floor.

This was discussed

with

the personnel

performing the task

who stated that this was to aid in

identification while performing the work and

was

a new management

initiative to improve job performance.

The inspector discussed

this

with the Haintenance

Hanager

who concurred

and stated that this practice

along with generally maintaining

a clean work area,

being prepared

to do

the work prior to starting, etc.,

would decrease

rework and ultimately

improve efficiency.

The inspector also discussed

this with the Health

Physics

supervisor

who stated that, with the efficiency increases,

overall

dose

expended

in maintenance

was expected

to drop.

The

inspector

concluded that these efforts were prudent

and that benefit

could

be attained

from them.

Conclusions

The licensee

reacted

properly to the subject

check valve failure.

Engineering evaluations

properly supported operability determinations.

10

RCS Walkdown

71707

Scope

On July 20, the inspector

accompanied

the licensee

on

NOP/NOT walkdowns

of the Unit

1 containment prior to return to service

from the Unit

1

outage.

Prior to the walkdown, the inspector

reviewed completed

procedure

OP 1-0120022,

revision 22, "Reactor Coolant

System

Leak Test,"

which reported

the results of the walkdowns performed at the beginning

of the outage,

and Technical

Department

Procedure

I-IPT-07, revision 3,

which described

the walkdowns to be performed.

Findings

With respect to the walkdowns conducted

at the beginning of the outage,

the inspector

noted that

a number of valve packing leaks

had

been

identified in the previous

walkdown and that

no pressurizer

nozzle leaks

were identified.

Personnel

performing the walkdowns documented

findings

in accordance

with the procedural

requirements

and documented

WOs

generated

as

a result of the findings appropriately.

With respect

to the post-outage

NOP/NOT walkdown, the inspector

attended

the pre-job briefing and found that topics,

including heat stress

limitations, required retest

inspections,

and tour path,

were covered

appropriately.

The inspector verified that the

RCS

had

been at

NOP for

at least

4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />,

as required

by procedure.

The inspector followed

portions of the walkdowns

and found that the licensee's

personnel

diligently ensured

that required inspections

were performed.

No

RCS

leakage

was identified as

a result of the inspections.

During the walkdowns,

the inspector

performed

independent

observations

of the state of containment cleanliness,

inspecting for foreign

materials

which might impede satisfactory

post-LOCA recirculation.

Previous

NRC inspections

in this regard

had indicated that the licensee

had performed marginally in establishing

containment cleanliness.

Following the recent Unit 2 outage,

the

NRC identified that the

licensee's

efforts had resulted

in a better level of cleanliness.

During this most recent inspection,

the inspector

found that the

containment

had

been returned to an excellent state of post-outage

cleanliness,

indicating that the licensee

has continued to improve in

the effectiveness

of removing material

from containment.

Conclusions

The inspector

concluded that pre

and post-outage

NOP walkdowns of the

RCS

had

been

performed satisfactorily.

Additionally, the inspector

found that the post-outage

cleanliness

of the Unit

1 containment

was

excellent.

ll

H2.3

Rod Control

S stem Maintenance

62703

M2.3.1

H2,3,2

Scope of Review

The licensee

has experienced

a series of recent

CEA drop events

due to various Control

Element Drive Hechanism

and related control

and instrumentation failures.

The inspector

reviewed the

licensee's

maintenance

program for the

Rod Control

Systems

to

determine

adequacy of preventive

and corrective maintenance

activities performed

on the systems.

Due to significant

differences

in system design

between Unit I and Unit 2 each unit

Rod Control

System is assigned

to separate

System Supervisors

and

separate

maintenance

crews.

Additionally, the inspector

determined that the licensee

conducts

an extensive

preventive

maintenance

program

on these

systems.

Routine maintenance

includes periodic performance of CEA coil current traces, circuit

and coil insulation resistance

checks

and power supply breaker

testing.

Current Traces

H2.3.3

The licensee

performs routine coil current traces of each

CEDH.

These traces

are normally scheduled

concurrent with planned

CEA

motion.

Additionally current traces

are often performed for

individual

CEAs during troubleshooting activities.

In this case

an evaluation of the trace

can

be used

as

an aid in diagnosing

circuit or rod motion problems.

Coil current traces

represent

a

signature

record for actual

current loading

on each of the coils

throughout the complete withdrawal

or insertion

sequence

and serve

as the best available indication of CEDM and

CEDMCS performance.

Traces

are evaluated for indications of potential

CEDM and

CEDMCS

problems

such

as

CEDH coil grounds or faulty CEDMCS components.

Evaluation of traces is performed

by one of the two system

supervisors.

Both personnel

have considerable

experience

in this

area

and demonstrated

good working knowledge of expected

current

traces

and system performance.

This information serves

as the

basis for licensee

decisions

in planning of troubleshooting

and

repairs during refueling outages.

The licensee

had previously

performed this testing in conjunction with scheduled

CEA motion

prior to and following each refueling outage.

However the

inspector

was informed that the licensee

had recently changed

their program to perform this testing every

90 days.

Circuit and Insulation Resistance

Checks

The licensee routinely performs circuit and insulation resistance

checks

on the

CEDHs.

These resistance

checks

are performed

from

the rod control cabinets

and provide the licensee

information

about the condition of the

CEDM coil stacks

and

CEDM cables.

12

Circuit Breaker Testing

The licensee

perforate

periodic testing of Rod Control

System

power

supply circuit breafers

to verify proper- operation

along with

correct overcurrent

and undervoltage

protection settings.

The

inspector determined that the licensee tests

25% of these circuit

breakers

each

outage.

Test Stand

The inspector

toured the licensee's

maintenance

training

facilities.

During this tour the inspector

observed

the

licensee's

CEDMCS test stand.

This test

stand is constructed

from

additional

Rod Control

System cabinets

and other components

procured for this purpose.

The test stand consists of a single

CEA coil stack with a modified/shortened

CEDH, power supply,

and

complete set of CEDMCS components

to allow moving the shortened

CEDM through the withdrawal

and insertion

sequences.

This

equipment is located outside the plant with other training

facilities and

was originally setup for training operations

and

maintenance

personnel.

However, it is also

used

by I&C

maintenance

personnel

as

an aid in troubleshooting

problems with

rod control components.

CEDHCS modules

suspected

of causing

problems

can

be removed

from the plant cabinets

and installed in

the test stand to determine

actual

source of the problem.

Corrective Maintenance

The inspector requested

that the licensee

provide

a list of all

corrective maintenance

performed

on the

Rod Control

Systems for

both units for the previous

two years.

The inspector

reviewed the

list and noted that the list included

a few WOs which specifically

addressed

dropped

CEAs,

some failure of CEAs to move, position

indication problems,

and various

component failures.

Additionally, numerous

WOs had

been

issued to correct problems

identified during predictive maintenance

(current traces

and

resistance

checks).

The inspector selected

several

completed

Work Orders

from this

list for review.

The Work Orders

were reviewed to determine the

adequacy of the licensee's

corrective maintenance,

and if the

maintenance

was successfully

performed within required Technical

Specification

allowed time limits.

Additionally the work

documents

were reviewed to determine if the licensee identified

any adverse

equipment

performance

trends for the

Rod Control

System

and initiated appropriate

actions to assess

the cause of

the trends.

The following WOs were reviewed:

~

WO 96005094-01

This

WO was issued

by the licensee

on

February

22,

1996, to investigate

the cause of CEA No.

20

dropping while Unit I was operating at power.

During

troubleshooting

licensee

personnel

determined that

a Power

13

Switch

SCR for the

CEA upper gripper

had shorted

causing

a

blown fuse.

Since the shorted

SCR could not be replaced

within the time allowed by Technical Specifications

the unit

was shutdown

and the defective

SCR was replaced.

~

WO 96005779-01

This

WO was issued

by the licensee

on March

1,

1996,

due to

apparent

rapid movement of CEA No.

1 on

Unit 1.

Operators

had noted indication of excessive

CEA

movement

between

129 and

133 inches with only slight

deflection of the control stick.

The

IEC technician

removed

the timer module

and lift power switch for CEA No.

1

and

tested

them on the test

bench.

The components

tested

as

acceptable.

The components

were reinstalled

and

a current

trace

performed during rod motion.

The current trace did

not

show any problems with the

CEDMCS.

However the

CEA

continued to indicate rapid motion between

129 and

133

inches.

The problem was subsequently

found to be

an

indication problem due to

a faulty position indication reed

switch rather than

a problem with actual

rod motion.

The

faulty reed switch was scheduled

to be replaced

during the

next outage.

The inspector verified that the reed switch

had subsequently

been replaced

under

PWO 3690.

~

WO 96011024-01

This

WO was issued

by the licensee

on April

28,

1996,

due to problems with moving

CEA No.

1

on Unit 1.

This

CEA was experiencing unreliable rod motion with both

withdrawal

and insertion

commands.

The licensee

determined

that the timer, pulldown power switch,

and lift power switch

modules

were defective.

The modules

were replaced

and

functionally tested satisfactorily.

~

WO 96012576-01

This.WO was issued

by the licensee

on May

13,

1996,

due to out of specification resistance

readings

on

the lower gripper coil and cable for CEA No.

2 on Unit 1.

During routine coil resistance

checks

the licensee

determined that the

CEA had higher than expected coil

resistance.

The licensee

cleaned

the pins

on both ends of

the

CEDH cable

and reterminated

the cable

and rechecked

the

resistance.

After cleaning the coil cable resistance

was

found to be acceptable.

~

WO 95004938-01

This

WO was issued

by the licensee

on

February

16,

1995,

due to

CEA No.

79 not stepping

out

smoothly

on Unit 2.

Licensee

personnel

identified

a faulty

ACTM board associated

with the

CEA.

The

ACTH board

was

replaced

and

FLCEA rod testing performed including monitored

CEDM coil current traces while operations

withdrew and

inserted

the

CEA with satisfactory results.

WO 95033292-01

This

WO was issued

by the licensee

on

November 25,

1995, to replace

a defective connector

socket

on Control Cabinet

2 on Unit 2.

The connector

socket

was

replaced

on December

4,

1995,

and satisfactorily tested

on

December

14,

1995.

~

WO 96012752-01

This

WO was issued

by the licensee

on May

16,

1996, to investigate

and repair

a reported defect with

loss of phase for CEA No.

49 on Unit 2.

Licensee

personnel

removed various

CEDMCS Power Switch components for the

CEA

and tested

them in the test stand.

The licensee

determined

that the optical isolator board

had failed.

The board

was

replaced

and satisfactorily tested.

Vendor Bulletins

The inspector

reviewed the status of the licensee's

program for

evaluation

and implementation of vendor recommendations

related to

the Control

Rod Drive System.

As part of this review the

inspector

held discussions

with the St.

Lucie ABB-Combustion

Engineering Site Representative.

During these

discussions

the

inspector

was informed that vendor recommendations

are provided to

sites

through

a series of ABB-CE Technotes

and

ABB-CE

Infobulletins.

The inspector

reviewed the listing of all

Technotes

and Infobulletins issued

by ABB-CE since

1979

and

determined that only a few related to the Control

Rod Drive

System.

The inspector identified

a single item, Infobulletin 89-

02, which

described

a potentially significant problem related to

multiple dropped

CEAs at another site.

Infobulletin 89-02 was

issued to inform plants of a multiple

CEA drop/slip event that

had

occurred at Palo Verde Unit

1 on December

10,

1988.

Additionally

the Infobulletin recommended

that licensee

management

evaluate

the

potential for CEA slip or drop at their site due to

a single fault

intermittent ground of a

CEDM coil lead during

CEA stepping.

The

specific problem at Palo Verde had

been

due to

a break in

insulation in

a

CEDM lower lift coil electrical

lead which

permitted intermittent arcing between

the coil lead

and

an

adjacent nipple assembly

during

CEA stepping.

During

a subsequent

meeting with licensee

personnel

the inspector

was informed that ABB-CE vendor recommendations

were included

within the scope of the licensee's

Nuclear Experience

Review

program.

The inspector

requested

that licensee

personnel

provide

documentation

to demonstrate

satisfactory disposition of ABB-CE

Infobulletin 89-02.

The inspector

was provided

a documentation

package for this issue.

This documentation

package

was reviewed

by the inspector.

The inspector determined that the licensee

had

evaluated

the Palo Verde event

and determined that the issue

was

not applicable to St.

Lucie due to significant different designs

and operational

history.

This determination

was

based

on the

CEDMCS utilized at both St. Lucie units differing from the unique

design utilized at Palo Verde while neither unit at St.

Lucie has

the additional

lower lift coils.

Additionally Unit 2 had operated

through it's first fuel cycle with multiple grounded

CEDM coil

circuits due to faulty coil field cable design.

No multiple CEA

M2.3.8

M2.3.9

15

drops

were experienced.

The faulty CEDM coil field cables

were

subsequently

replaced.

The inspector determined that the licensee

had

an adequate

program for addressing

vendor recommendations

for

the Control

Rod Drive System.

Walkdown of System

Components

The inspector

performed

a walkdown of portions of the Saint Lucie

Rod Control

Systems.

Included in the walkdown were the Reactor

Trip Breakers,

CEDMCS power supplies,

and rod control cabinets for

Unit

1

and Unit 2.

No significant problems

were noted during this

tour and housekeeping

within cabinets

was acceptable.

Conclusions

The licensee's

preventive

maintenance

program for the

Rod Control

Systems

was adequate.

Corrective maintenance activities reviewed

by the inspector

were acceptable.

Additionally, the licensee's

decision to increase

the

amount of predictive maintenance

on these

systems

has contributed

toward

a reduction in the number of CEA

drop events

and less failures of system

components

during reactor

operation.

M3

Maintenance

Procedures

and Documentation

~

~

M3. 1

A lication of Freeze

Seals

62703

a

0

b.

Scope

The inspector

reviewed

GMP-10, revision 6, "Application Of Freeze

Seals,"

and several

work orders

completed during the recent Unit

1

refueling outage involving the

use of freeze seals,

Find'ings

The inspector

found that the procedure

contained

appropriate

guidance to

preclude

challenges

to the plant associated

with the use of freeze

seals.

Documentation

reviews of the following work orders

were

completed

as delineated

below.

All the packages

contained

the required

documentation

including implantation plans,

contingency plans,

inspection reports,

and temperature

monitoring logs.

Exceptions

are

as

noted below:

Work Order 96008441 installed

a freeze

seal

on

a six inch SI

system

header.

The temperature

monitoring log had

been maintained

as

suggested

in the procedure;

however,

the inspector

noted two

periods of time on May 22 in which the readings

were not

documented.

In one case

a reading

suggested

to be taken every

twenty minutes

was not recorded

and in another

case

the reading

was taken every thirty minutes.

16

~

Work Order 96005107 installed

a freeze

seal

on another six inch SI

system

header.

The temperature

monitoring log had

been maintained

as

suggested

in the procedure,

however,

the inspector

noted for a

period of one hour on May 22 that

no readings

were documented.

~

Work Order 96008029 installed

a freeze

seal

on

a twelve inch SI

system line.

~

Work Order 96005109 installed

a freeze

seal

on

a six inch SI

system

header.

~

Work Order 96011512 installed

a freeze

seal

on

a 3/4 inch

RCS

instrumentation line.

The inspector discussed

the cases

involving readings

not logged with a

maintenance

supervisor

involved with freeze

seal

usage.

He stated that

recording the readings

every twenty minutes is

a guide

and not

a strict

procedural

requirement.

He further stated that the freeze

seals

were

never left unattended

and the readings

were probably not recorded

simply

because

the freeze

seal

attendant

forgot to do so.

Discussion with licensee

management

indicated that for a short period of

time, approximately

one hour,

work had

been

stopped to clean the area of

trash

and unnecessary

equipment.

Although the freeze

seal

personnel

were not located directly at the freeze

seal

they were in the area to

fulfillcontingency requirements, if necessary.

However, after further

discussion

with the Maintenance

Manager,

the inspector

concluded that,

although the freeze

seal

monitor was in -the area,

he was not actively

monitoring the seal

as evidenced

by the absence

of freeze

seal

temperature

data for the time in question.

This was

a violation of the

licensee's

procedure

which requires that at no time shall

a freeze

seal

be left unattended

for any reason until the system or component is

restored

or the Contingency

Plan is implemented.

However, this failure

constitutes

a violation of minor significance

and is being treated

as

a

Non-Cited Violation, consistent

with Section

IV of the

NRC Enforcement

Policy

(NCV 335/96-11-03,

"Failure To Properly Monitor Freeze

Seal" )

The inspector

reviewed the control

room logs

and noted that there were

no log entries

which would indicate that the freeze seals

were left

unattended.

In addition, the inspector verified that the thaw time of

each of these

seals

would have

been

on the order of two to three

hours

and therefore

concluded that the safety

impact

was minimal.

Conclusion

A review of freeze seals

applied during the recent Unit

1 outage

indicated that procedural

requirements

had not been

met in one case.

M8.1

17

Miscellaneous

Maintenance

Issues

(62703)

LER 389 96-001

"Manual Reactor Tri

Due to Hi

h Main Generator

Cold Gas

Tem erature"

a

~

b.

Scope

The subject

LER discussed,

in part,

anomalous

level indications in Unit

2

SGs following a unit trip.

The indications

were the result of

blockage

in the sensing lines to level transmitters for the

SGs.

As

part of their corrective actions,

the licensee

committed to performing

blowdowns of the Unit

1

SGs during the next outage of sufficient length.

Findings

The inspector

reviewed completed

WO 96008361

01, prepared

to perform the

subject

blowdowns.

The

WO invoked procedure

I-IMP-09.07, which was

prepared

to direct the blowdown evolutions.

The inspector

found that

the blowdowns

had

been

performed consistent

with the licensee's

commitments.

C.

Conclusion

The licensee satisfied their commitments with respect

to blowing down

the Unit

1

SG level sensing lines.

III. En ineerin

El

E1.1

Conduct of Engineering

UFSAR

U date

Pro

ram

37550

a ~

Inspection

Scope

The inspectors

reviewed the adequacy of the licensee's

program for

reviewing their

UFSAR and evaluated

the corrective actions

taken for

these identified items.

b.

Observations

and Findings

As

a result of

a boron dilution event

on January

22,

1996, that resulted

in a violation/civil penalty,

the licensee

committed to several

long

term corrective actions.

One of these corrective actions

was to perform

a comprehensive

review of compliance with the

UFSAR.

The purpose of

this review was to evaluate

the

UFSAR and to make the changes

identified.

At the time of the inspection

(July 22-26,

1996) the licensee

had

reviewed approximately

one third of the

UFSAR.

Most of the review was

for Unit

1

UFSAR and

was in the text material

not for tables

and curves.

Approximately

170 findings

and

500 editorial errors

were identified in

this evaluation.

None of these findings were determined

to be

operability problems.

18

C.

The inspectors

reviewed the procedure

being used,

the experience

and

technical discipline of the reviewers,

some of the

UFSAR findings and

related corrective actions,

root causes/corrective

actions,

and process

improvement for future use/reviews

of the

UFSAR.

On July 26,

1996,

the

licensee

had not made

a decision

on the extent

and details of the

remaining review for the

UFSAR.

Conclusions

on Conduct of Engineering

The inspectors

did not identify any problems with the licensee's

review

of the first one third of the

UFSAR.

E2

E2.1

Engineering

Support of Facilities

and Equipment

Prelubrication of Valves Prior to Testin

37551

92902

a

~

Scope

In August,

1995,

an

NRC inspector identified, through document

review,

that the Unit

1 containment

spray flow control valve,

1-FCV-07-1A,

was

being preconditioned prior to being tested.

Specifically, prior to the

performance of the surveillance

which verified proper stroke-time of the

valve, lubrication was applied to the valve stem.

Further inspection

identified that three other containment

spray valves were also

prelubricated, prior to being stroke-time tested.

As the inspectors

could not identify a clear violation resulting from

the practice of prelubrication at the time the practice

was identified,

a TIA was prepared

requesting

NRR to provide

an interpretation of the

code with respect

to the practice.

During the current inspection

period,

a response

was received

which stated that the practice

was in

violation of 10 CFR 50 Appendix B, Criterion XI requirements

that

testing

be performed

under suitable environmental

conditions

(the thrust

being that prelubrication altered

the environmental

conditions of the

test

such that the test could not assess

the ability of the valves to

perform their intended function).

b.

Findings

The licensee

had noted in a guality Assurance

(gA) assessment

that this

practice

was occurring;

however, it was not highlighted

as significant

nor was

a St.

Lucie Action Request

(STAR) written to document its

occurrence.

The

gA assessment

indicated that there did not appear to be

a correlation

between

frequency of lubrication

and test performance.

However,

when informed by the inspector that this practice could result

in not obtaining true as-found data

and would not provide reliable trend

information, the licensee

agreed

and revised the appropriate

procedures

to delete

the practice.

Violation 335/95-15-05

was issued

documenting

the fact that

a

STAR was not initiated as required

by plant procedures.

19

Corrective actions for this violation included documenting

the event in

STAR 951048

as well as revising the applicable

procedures

to remove the

practice of prelubricating other valves prior to surveillance testing.

In addition,

STAR 951063

was written to review other test

and

surveillance

procedures

to determine if similar conditions existed

elsewhere.

One additional

valve was identified that might be impacted

by this practice

and that problem was also corrected.

The licensee

stated,

in response

to

STAR 951063, that the

PMs which lubricated the

valves were performed

along with the stroke-time surveillance

because

the surveillance

was required

as

a

PMT following the

PM.

By scheduling

the

PM to be performed prior to the surveillance

the number of

surveillances

performed would be reduced.

The inspectors

reviewed stroke time testing data for the subject valves.

The reviews

examined the stroke times both before

and after the practice

of prelubrication

was initiated.

The inspectors

found that

no

identifiable change

in stroke times resulted

from the initiation of the

practice.

However, the inspectors

found that the failure of the

licensee's

procedure

change

review process

to identify the potential

impact of the change

(the addition of preconditioning)

indicated

a

weakness

in the process.

10 CFR 50, Appendix 8, Criterion XI, requires,

in part, that testing

required to demonstrate

that systems

and components will perform

satisfactorily in service shall

be performed

under suitable

environmental

conditions.

Prelubrication of valves prior to performing

stroke-time tests violates this requirement

and negates

the validity of

the test in assessing

the operational

readiness

of the valve,

and is

being identified as

VIO 335/96-11-04,

"Preconditioning of Valves Prior

to Surveillance".

Control

Element Drive Mechanisms

and Related

Control

and Instrumentation

Ins ection

Sco

e

37550

Due to the number of recent control element

assembly

(CEA) drop events

the inspector

reviewed these

and past events to determine if engineering

support to the system

was appropriate.

There were four CEA drop events

in 1996, three

on Unit

1 and

one

on Unit 2.

The

CEAs are

one of the

systems

which are

used to control core reactivity through insertion or

withdrawal of absorption

rods.

The scope of the inspection

was to

review the cause

determinations

and corrective actions for these

problems.

Historical information on dropped

CEA events

and system

upgrades

were reviewed.

Maintenance activities were also reviewed,

and

that portion of the inspection is covered in Section

M2.3.

Observations

and Findin

s

On Unit 1, the control

equipment for the control element drive

mechanisms

consisted

of discrete electronic

components.

On Unit 2, the

control equipment

was

a later version consisting of integrated circuits,

and

was referred to as the Advanced Control Timing Mechanism.

Unit 2

control equipment

incorporated

a feedback

(or checkback) circuit which

had the capability of blocking all movement signals if an error was

detected.

The

CEAs have

been operated

in manual

mode only.

20

Dropped

CEA events that occurred

between

the beginning of 1993

and the

time of this inspection

are

summarized

below.

DROPPED

CEA EVENTS JANUARY 1993

TO JULY 1996

Unit

CEA No.

Date

Cause

2

12

5/24/96

Unknown, suspect

bumped fuse.

1

1

3/4/96

Operator error, quick release

of bypass

switch.

47

20

63

2/23/96

Loose connection

in interconnecting

wiring.

2/22/96

Failed (i.e. shorted) silicon controlled

rectifier (SCR) in A phase

upper gripper

switch module causing

fuse to open.

11/1/93

Timer card not seated.

8/26/93

Unknown.

5/21/93

Ground faults at containment

penetration

coupled with failed circuit breaker.

Seven

CEAs dropped.

In all but two cases,

the root causes for the dropped

CEAs were

determined

and corrected.

In the two cases

where the root cause

was not

definitely established,

a momentary perturbation

in the timing sequence

was suspected,

and those

CEAs have operated correctly thereafter.

Review of statistics

on dropped

CEA events

and their causes

would

indicate that the Unit 2 system

has

been

more reliable than Unit 1.

Since at least

1990, with the exception of one

unknown cause,

the Unit 2

dropped

CEA events

were caused

by problems outside the boundary of the

control hardware.

The inspector

concluded that these

problems

would not

be expected

to recur in the future.

These facts support the licensee's

contention that the Unit 2

CEA System

has

been highly reliable.

However, this conclusion

based

on St.

Lucie specific data

was in

conflict with data obtained

from a broader

base.

Data gathered

by

Combustion

Engineering

on dropped

CEA events at all plants

where

CE was

the

NSSS supplier would indicate that the Unit 2 class of equipment

has

not been

as reliable

as the Unit

1 class

equipment.

The multiple dropped

CEA event

on Unit 2 in Nay 1993

was caused

by

insulation

breakdown of multiple conductors

at the containment

penetration

together with a failed

CEA circuit breaker.

The penetration

problem appeared

to be

an isolated

case.

The circuit breaker that

fai,led was

a four pole breaker.

The failure mode of the circuit breaker

was failure of two poles to open,

which resulted

in tripping of the

upstream

sub-group circuit breaker.

C.

21

Overall, the

known causes

of the dropped

CEA events listed in the above

table are all different.

Therefore,'he

data

does not indicate

any

negative

component

nor personnel

related trend.

The only modification implemented to upgrade

the reliability of the

CEA

System

has

been the changeout

of the

CEA 15

VDC power supplies with

power supplies built to

a stricter specification.

This modification has

been

completed

on Unit

1 during the current outage.

Also at Unit 1,

cables

which connect to the

CEAs themselves

(referred to as

head cables)

were replaced

during the current outage,

because

the prefabricated

connectors

were failing at

an increasing rate.

The licensee

has established

a team to analyze the

CEA System

reliability and propose

upgrades if warranted.

The team

had

a target

date of mid-September for issuance

of their report.

Conclusions

E2.3

The inspector

concluded that engineering

support

on

CEDHs

and related

controls

and instrumentation

was good.

AFAS Set pints

Found to be Nonconservative

37551

'cope

On July 18, Unit

1 operators

noticed that the

0 channel

level indicator

for SG

18 was indicating

3 to

4 per cent lower than the balance of SG

level channels.

CR 96-1768

was initiated to document the condition.

The inspector followed the licensee's

activities in response

to this

issue.

b.

Findings

In evaluating control

room observations,

engineering

personnel

determined that calibrations

performed

on the Unit

1

SG level

transmitters,

performed

as

a result of higher than expected

SG tube

plugging (which resulted

in different saturation

conditions in the

SGs

and

a subsequent

change

in

SG water density) during the ongoing

refueling outage

may have

used nonconservative

values for elevations

considered for the transmitters'eference

legs.

Specifically,

a

concern

arose that elevations for reference

leg taps

may have

been

used

in the development of calibration data,

as

opposed to as-built data

on

the elevations of the condensate

pots which provided the reference

columns for the transmitters

in question.

In parallel with the engineering activities

on the issue,

the licensee

proceeded

to modify the setpoints for AFAS actuation

from their existing

setpoints of 19.5 per cent to 24.5 per cent of narrow range.

PC/H 96-

119 was generated

to affect the setpoint

change with the goal of

ensuring that adequate

margin would exist between

the

new (24.5 per

cent) setpoints

and

any correction (resulting from the engineering

reviews being conducted)

to ensure that the

TS minimum allowable

AFAS

22

setpoint of greater

than or equal to 18 per cent

was not violated.

With

the unit in Mode 3 at the time,

TS required that

a minimum of 3 AFAS

channels

be operable or that, for only 2 channels

operable,

that

one

channel

be tripped

and

one channel

be in bypass within one hour.

If

more thar, two channels

were inoperable,

TS required that the unit be

placed in Mode

4 per

TS 3.0.3.

The

new setpoints

were established

on

July 19.

After setpoints

had

been elevated,

the licensee

determined,

based

upon

the results of field inspections

of the as-built locations of condensate

pots, that nonconservative

errors existed

in the following level

channels:

~

SG

1A

~

LT-9013C - . 1%

~

LT-9013D - . 8%

~

SG IB

~

LT 9023A

3.0%

~

LT-9023B -2.9%

~

LT-9023C -1.7%

c.

Conclusion

At the close of the inspection period, the licensee

was still

investigating the cause for the erroneous

calibration data.

As

additional, root cause-related,

information was required to determine

whether violations of NRC requirements

occurred, this issue will be

tracked

as

an unresolved

item (URI 50-335/95-11-05,

"Discrepancies

in

AFAS Calibration Data" ).

E2.4

Unit

1 Nuclear Instrumentation

Wirin

Errors

37551

a

~

Scope

On July 30, with Unit

1 at

100% power, the licensee identified

a

discrepancy

involving wiring errors in the safety,.related

linear NI

channels.

The errors resulted

in channels

A, C,

and

D reporting ASI

values

which were opposite of true values; that is,

an apparent wiring

error had reversed

upper

and lower detector

inputs to the NI drawers

such that ASI was misclculated.

The inspectors

followed the licensee's

activities relating to this event.

,

Findings

23

C.

At 1:00 p.m., Unit

1 operators

declared

the A, C,

and

D channels

OOS,

which placed the unit in TS 3.0.3

due to 3 of 4

RPS channels for THLP

and

LPD, which received

ASI inputs,

being inoperable

due to the

erroneous wiring.

The inspector

responded

to the control

room and found

that leads

were being reversed

on the

A and

C channels

in, an attempt to

restore

the channels

to operability.

Reactor

Engineering

support

was

available,

with new NI gain values

being calculated

in support of I8C as

the leads for the affected

channels

were properly aligned.

At 1:50 and

2:00 p.m.,

work was completed

on the

A and

C channels,

respectively,

and

operators

drove

CEAs into the core to verify proper ASI response.

The

inspector verified that proper channel

response

occurred,

and the

A and

C channels

were declared

operable

at 2:00 p.m., leading to an exit from

TS 3.0.3.

The inspector

found that

I&C and Reactor

Engineering

response

was timely in preventing

a unit shutdown.

The apparent

root cause for the wiring errors

was errors in

CWDs

prepared for the Unit

1 NI upgrade.

The affected

CWDs conflicted with

the

VTH for the NI drawers

being installed, resulting in wiring errors.

The licensee's

root cause

investigation

was proceeding

at the close of

the inspection period,

as

was the inspectors'eview

of the event.

As

more information on root cause

was required to properly assess

the

failures leading to this event,

the continued inspection efforts will be

tracked

as

an 'unresolved

item (URI 335/96-11-06,

"Unit

1 NI Wiring

Errors" ).

Conclusion

Operators

properly characterized

the effects of the subject wiring

errors

on system operability.

I8C and Reactor Engineering

support in

preventing

a unit shutdown

was timely.

The root causes

of the event

will be tracked

as

an unresolved

item.

E7

E7.1

guality Assurance

in Engineering Activities

ualit

Assurance

in

En ineerin

Activities

37551

a

~

b.

Inspection

Scope

A review was performed

on the failure to replug

one of the steam

generator

tubes

and the failure of the vendor's quality group to detect

this problem.

Observations

and Findings

The licensee's

final review of the Unit

1

B steam generator

tube

plugging documentation

(on July 7,

1996)

by the Components/Supports

Inspection

Group

(CSI) identified that the vendor

had failed to replug

a

tube in the hot leg.

Additional discrepancies

were found by the vendor,

e.g.,

two stakes

used for whip restraints

were not installed.

The

licensee

gA group found two installed stakes that were not required.

C.

E8

E8.1

24

The licensee's

gA Independent

Technical

Review Group

( ITR) initiated

an

assessment

of the discrepancies,

The inspectors

reviewed the

preliminary results of this assessment

and considered it to be very

thorough.

A finding was issued

in licensee

surveillance

number

08.06.CEPSG.96.7

for failure to follow procedure with four examples,

e.g., failure to plug tube, failure to adequately transfer staking

information, etc.

Also, four recommendations

addressing

opportunities

for improvement

and concerns

identified during the

ITR Groups

independent

technical

reviews were issued.

The finding will have to be

answered

by the tube plugging vendor

and

some of the recommendations

and

concerns will be addressed

by some of the license'e

groups.

Conclusions

on guality Assurance

in Engineering Activities

The licensee's

CSI engineering

group

and the

gA ITR group performed

thorough inspections

and assessments

of the tube plugging process

that

resulted

in

a finding, recommendations,

and concerns.

The vendor

completed

the required work as

a result of the actions

by the licensee

groups.

Hiscellaneous

Engineering

Issues

(37551)

LER 50-389-95-005

"2A Emer enc

Diesel

Generator

Rela

Socket Failures

Due to Hi

h

C cle Fati

ue"

The subject

LER documented

the failure of the

2A

EDG to start locally

and

a subsequent

failure to operate

properly due to solder cracks

and

connection failures associated

with relay sockets.

Critical Unit 2

sockets

were replaced

at the time,

and

a commitment

was

made to replace

similarly susceptible

sockets

on Unit

1 during the next Unit

1 outage.

The inspector

reviewed

PC/N 030-196M, revision 0,

"EDG Relay

and

Mounting Socket

Replacement,"

which was executed

during the current Unit

1 outage.

Under the

PC/N, existing Curtis

RS-11 relay sockets/mounting

tracks

and Square

D KPD-13 relays

were replaced with new components.

The activities were affected

under

PWOs 96009958

01

and

96009957

01

and

were completed

June

8 for the

B train

EDG and

Nay

21 for the

A train

EDG.

These activities satisfied

the licensee's

commitments

under the

subject

LER.

This

LER remains

open pending completion of the licensee's

corrective actions

stated

in the

LER.

E8.2

Shutdown Coolin

Relief Valve Set oint Chan

es

IR 95-20 documented

an event in which

a shutdown cooling discharge

relief valve lifted and failed to reseat,

resulting in an approximate

4000 gallon loss of RCS inventory.

The cause of the event

was

a

nonconservatively

low lift setpoint,

combined with an excessive

blowdown

setting which resulted

in an inability of the valve to reseat

once

lifted.

One corrective action in response

to VIO 335,389/95-20-01,

"Failure to

Promptly Correct Conditions Adverse to guality," involved establishing

25

new setpoints

for Unit

1 relief valves

V-3468 and V-3483 (the

SDC

suction reliefs) from the existing 320 psig setpoint to 330 psig.

The

changes

were affected

under

PC/H 014-196, revision 0,

"Shutdown Cooling

Relief Valves V-3468 and

V3483 Set Pressure

Increase."

The inspector

reviewed the licensee's

completed

package

and found that the changes

were affected consistent with the licensee's

commitments.

V. Kana ement Neetin

s and Other Areas

Xl

Exit Heeting

Summary

The inspectors

presented

the inspection results to members of licensee

management

at the conclusion of the inspection

on August 6.

The

licensee

acknowledged

the findings presented.

The inspectors

asked

the licensee

whether

any materials

examined during

, the inspection

should

be considered

proprietary.

No proprietary

information was identified.

5

26

PARTIAL LIST OF

PERSONS

CONTACTED

Licensee

W. Bladow, Site guality Manager

H. Buchanan,

Health Physics Supervisor

C. Burton, Site Services

Manager

R.

Dawson,

Business

Manager

D. Denver, Site Engineering

Manager

R. Frechette,

Chemistry Supervisor

P. Fulford, Operations

Support

and Testing Supervisor

C. Harple, Operations

Supervisor

K. Heffelfinger, Protection Services

Supervisor

J. Holt, Information Services

Supervisor

H. Johnson,

Operations

Manager

T. Kreinberg,

Nuclear Material

Management

Superintendent

J.

Harchese,

Maintenance

Manager

C. O'Farrel,

P, actor Engineering Supervisor

R. Olson,

Instrument

and Control Maintenance

Supervisor

C. Pell,

Outage

Manager

J. Scarola,

St.

Lucie Plant General

Manager

A. Stall, Site Vice President

E.

Weinkam, Licensing Manager

C.

Wood,

System

and

Component

Engineering

Manager

W. White, Security Supervisor

Other licensee

employees

contacted

included office, operations,

engineering,

maintenance,

chemistry/radiation,

and corporate

personnel.

IP 37550:

IP 37551:

IP 40500:

IP 62703:

IP 71707'P

71750:

IP 92902:

IP 93702:

~oened

27

INSPECTION

PROCEDURES

USED

Engineering

Onsite Engineering

Effectiveness of Licensee

Controls in Identifying, Resolving,

and

Preventing

Problems

Maintenance

Observations

Plant Operations

Plant Support Activities

Followup - Maintenance

Prompt Onsite

Response

to Events at Operating

Power Reactors

ITEMS OPENED,

CLOSED,

AND DISCUSSED

50-335/96-11-01

IFI

"Adequacy of Root Cause

Investigation for Unit

1

Charging

System Anomalies"

335,389/96-11-02

NCV

"Failure to Obtain Originator's Concurrence

During

STAR Closeout"

50-335/96-11-03

50-335/95-11-05

50-335/96-11-06

Closed

335/96-11-04

Discussed

389/96-001

50-389-95-005

NCV

"Failure To Properly Monitor Freeze

Seal"

URI

"Discrepancies

in AFAS Calibration Data"

URI

"Unit

1 NI Wiring Errors"

VIO

"Preconditioning of Valves Prior to Surveillance"

LER

"Manual Reactor Trip Due to High Main Generator

Cold

Gas Temperature"

LER

"2A Emergency

Diesel

Generator

Relay Socket Failures

Due to High Cycle Fatigue"

335,389/95-20-01

VIO

"Failure to Promptly Correct Conditions Adverse to

guality"

'

ACTH

AFAS

AFW

ASI

CE

CEA

CEDM

CEDHCS

CET

CFR

CR

CWD

DPR

EDG

FCV

FLCEA

FR

FRG

GMP

gpm

HPSI

IFI

IR

ITR

LOCA

LPD

LPSI

LT

NCV

NI

NOP

NOT

NSSS

OOS

OP

PC/H

PGM

PH

PHAI

PHT

Pslg

PSL

PWO

QA

QI

RCS

RPS

RRS

RTD

28

LIST OF ACRONYHS USED

Automatic

CEA Timing Module

Auxiliary Feedwater Actuation System

Auxiliary Feedwater

(system)

Axial Shape

Index

Combustion

Engineering

(company)

Control

Element Assembly

Control

Element Drive Mechanism

Control

Element Drive Mechanism Control

System

Core Exit Thermocouple

Code of Federal

Regulations

Condition Report

Control Wiring Diagram

Demonstration

Power Reactor

(A type of operating license)

Emergency

Diesel

Generator

Flow Control Valve

Full Length Control

Element Assembly

Flow Recorder

Facility Review Group

General

Maintenance

Procedure

Gallon(s)

Per Minute (flow rate)

High Pressure

Safety Injection (system)

[NRC] Inspector

Followup Item

[NRC] Inspection

Report

Independent

Technical

Review Group

Loss of Coolant Accident

Local

Power Density

Low Pressure

Safety Injection (system)

Level Transmitter

NonCited Violation (of NRC requirements)

Nuclear Instrument

Normal Operating

Pressure

Normal Operating Temperature

Nuclear

Steam Supply System

Out Of Service

Operating

Procedure

Plant Change/Modification

Plant General

Manager

Preventive

Maintenance

Plant

Management Action Item

Post Maintenance

Test

Pounds

per square

inch (gage)

Plant St.

Lucie

Plant

Work Order

Quality Assurance

Quality Instruction

Reactor Coolant System

Reactor Protection

System

Reactor Regulating

System

Resistive

Temperature

Detector

SCR

SDC

SG

SI

SNPO

SPDS

TE

TIA

TMLP

TS

UFSAR

URI

VDC

VIO

VTM

WO 29

Silicon Controlled Rectifier

Shut

Down Cooling

Steam Generator

Safety Injection (system)

Senior Nuclear Plant [unlicensed]

Operator

Safety

Parameter

Display System

Temperature

Element

Temperature

Indicator and Alarm

Thermal

Margin Local

Power

Technical Specification(s)

Updated Final Safety Analysis Report

[NRC] Unresolved

Item

Volts Direct Current

Violation (of NRC requirements)

Vendor Technical

Manual

Work Order