ML17202L299

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SALP Repts 50-237/90-01 & 50-249/90-01 for Feb 1989 - Apr 1990
ML17202L299
Person / Time
Site: Dresden  Constellation icon.png
Issue date: 06/29/1990
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17202L297 List:
References
50-237-90-01, 50-237-90-1, 50-249-90-01, 50-249-90-1, NUDOCS 9007100209
Download: ML17202L299 (34)


See also: IR 05000237/1990001

Text

I

-

SALP 9

INITIAL SALP REPORT

U. S. NUCLEAR REGULATORY COMMISSION

.REGION III

SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE

50-237/90001; 50-249/90001

Commonwealth Edison Company

Dresden Station

February 1, 1989 through Apri 1 30, 1990

'p

1 .***

I

.

  • ..,.

TABLE OF CONTENTS

Page No.

LIST OF ACRONYMS

I.

INTRODUCTION ............................. ~. . . . . . . . . . . . .

1

II.

SUMMARY OF RESULTS . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

2

A.*

Overview ....... * ...................... * ....... *.......

2

B.

Other Are~s of Interest ....................... *. ...

2

I I I. C.RlTERIA ; ..... * ........ , ...... .' ..... * . . :.. . . . . . . . . . . . . . . . . . .

3

IV.

PERFORMANCE ANALYSIS .... *...............................

5

A.

Plant Operations ............... *...................

5

B.

Radiological Controls . . . . . . . . . . . . . . . . . . . . . . . . . . . . .

8

C.

Mai ntenance/Surveil 1 ance . . . . . . . . . . . . . . . . . . . . . . . . . .

10

D;

Emergency Preparedness ......... : ...... ....... ;....

14

E.

Security .......................... *................

15

F.

Enginee~ing/Technical Support ...........

L **** ;~...

17

G.

Safety Assessment/Quality Verification ............

20

V.

SUPPORTING DATA AND SUMMARIES ................ : . . . . . . . . . .

26

A.

Licensee .Activities .................... ~..........

26

B.

Inspection Activities .......... *...................

28

C.

Escalated Enforcement Actions .....................

29

D.

Confirmatory ActionLe.tters (CALs) ..... : ..... :....

29

E.

Review of Licensee Event Reports ........... :; ..*.. *

30

i

)

  • ..
  • -

ACAD/CAM

AEOD

AIT

A LARA

ANSI

BOP

BWR

CCTV

CAL

CECO

CFR

DCRDR

DRP

DRS

DRSS

DSIP

ECCS

EPA

EDP

EPIP

EPRI

EP

EQ

ERO

ESF

FSAR

GE

HP

HPCI

HWC

IC

I GS CC

ILRT

IN

ISI

IST

kV

LER

LLRT

LPCI

MIP

MSIV

MSL

NOE

NRC

ACRONYMS

atmospheric containment atmosphere dilution/containment atmosphere

monitor

Office for Analysis and Evaluation of Operational Data

Augmented Inspection Team

as-low-as-reasonably-achievable

American National Standards Institute

balance-of-plant

boiling water reactor

closed circuit television

Confirmatory Action Letter

Commonwealth Edison Company

Code of Federal Regulations

Detailed Control Room Design Review

Division of Reactor Projects

Division of Reactor Safety.

Division of Radiation Safety and Safeguards

Dresden Station Imp_rovement Program

emergency core cooling system*

electrical protection assembly

emergency operating procedure -

Emergency Plan Implementing Procedures

Electric Power Research Institute

emergency preparedness

environmental qualification

Emergency Re~porise Organization

eng1neered safety feature

Final Safety Analysis Report

General Electric

health physics

high pressure coolant injection

hydrogen water chemistry

isolation condenser

interg~anular stress corrosion cracking

integrated leak rate test.

Information Notice

ins&rvice inspection

inservice testing

Kil ovo ltage

licensee event report

local leak rate test

low pressure coolant injection

maintenance improvement program

main steam isolation valve

main steam line

non-destructive examination.

Nuclear Regulatory Commission

ii

.. *** ....

..

NRR

NSO

PM

QA

QC

REM

REMP

RER

RO

RPS

SALP

SA/QV

SBO

SGTS

SMAD

SRO

TS

voe

Office of N~clear Reactor Regulation

nuclear station operator

preventive maintenance

quality assurance

quality control

roentgen equivalent man

Radiological Environmental Monitoring Program

Regulatory Effectiv~ness Review

reactor operator

.

reactor protection system*

Systematic Assessment of Licensee Performance

Safety Assessment/Quality Verification

Station Blackout

Standby gas treatment system

System Materials Analysis Department

senior reactor operator

Technical Specifications

Volts~Direct C~rrent

iii

i;.

I.

INTRODUCTION

The Systematic Assessment of Licensee Performance (SALP) program is an

integrated NRC staff effort to collect available observations and data

on a periodic basis and to evaluate licensee ~erformance on the basis

of this information.

The program is supplemental to normal regulatory

processes used to ensure compliance with NRC

rul~s and regulations .. It

is intended to be iufficiently diagnostic to provide a rational basis for

allocating NRC resources and to provide meaningful feedback to the licensee's

management regarding the NRC' s assessment of their facility's performance

in each functional area.

An NRC SALP Board, composed of- the staff members listed below, met on*

June 13, 1990, to review the observations and data on performance, and to

assess licensee performance in accordance with the guidance in NRC Manual

Chapter 0516, "Systematic Assessment of Licensee Performance."

The

guidance and evaluation criteria are summarized in Se~tion III of this .

report.

The Board's findings and recommendations were forwarded to the

NRC Regional Administrator for approval and issuance.

This report is the NRC's assessment of the licensee's safety performance

at Dresden.Station for the period February 1, 1989, ~hrough April 30, 1990.

The SALP Board for Dresden Station SALP 9 was composed of the following

individuals:

Board Chairman

-,

C. E. Norelius, Director, Division of_ Radiation Sa.fety -and.Safeguards (DRSS)

Board Members

E. G. Greenman, Director~ Division of Reactor Projects (DRP)

T. 0. Martin, Deputy Director, Division of Reactor Safety (DRS)

R.

F~ Dudley, Acting Project Director, Project Directorate III-2,

Office of Nuclear Reactor Regulation (NRR)

-

W. D. Shafer, Chief, Branch 1, Division of Rea~tor Projetts

a. L. Siegel, Project Manager, Project Directorate III-2, NRR

S. G. DuPont, Senior Resident Inspector

Other Attendees at the SALP Board Meeting

L; R. Greger, Chief, Reactor Programs Branch, DRSS

M. P. Phillips, Chief, Operational Programs- Seciion, DRS

W. G. Snell, Chief, Radiological Controls and Emergency Preparedness

Section, DRSS

-

J. M.

Hinds~ Chief, Projects Section 18, DRP

J. R. Creed, Chief, Safeguards S~~tion, DRSS _

D. Hills, Resident Inspector, DRP

D. Jones, Reactor Engineer, DRP

D. aarss, Emergency Preparedness Analyst, DRSS

T.- Madeda, Physical Security Inspector, DRSS

F. *Maura, Reactor In specter, DRS

II.

SUMMARY OF RESULTS

A.

Overview

This assessment period is from February 1, 1989 through

April 30, 1990 (15 months versus 12 months for the previous

assessment period).

Management involvement was generally evident

and resulted in improved overall performance.

Good performance

i.n the areas of Operations, Emergency Preparedness and* Security

demonstrated management effecti~eness. The licensee's

responsiveness to NRC initiatives and cohcerns was adequate with

some weaknesses regarding the quality and timeliness of corporate

licensing activities.

I

Resolution of technical issues was good.

Enforcement history

generally improved with no escalat~d enforcement actions taken.

Training and qualifications wa*s very good overall with the exception

of Engineering/Technical Support.

Staffing was adequate overall

with the exception of Engineering/Technical Support. *

The performance ratings during the previous assessment period and

this assessment period according to functional areas are given below:

Functional Area

Plant Operations

Radiological Controls

Maintenance/Surveillance

Emergency Preparedness

Security

Engineering/Technical Support

.. Safety Assessment/Quality

Verification

B. *

Other Areas of Interest

None.

2

Rating Last

Period .

1

2

2

  • 1

2 Improving

2

2 Improving

Rating This

Period

l.

2

2

1

1 .

2

2

Trend

Improving.*

" .

I I I. CRITERIA

Licensee performance is assessed in selected functional areas.

Functional

  • areas normally represent areas significant to nuclear safety and the

environment.

Some functional areas may not be assessed because of little

or no

licen~ee activities or lack of meaningful observations.

Special

a~eas may be add~d to highlight significant observations.

The following evaluation criteria were used to assess each functional

area:

1.

Assurance of quality, including management involvement and control;

2.

Approach to the identification and resolution of technical issues

from a safety standpoint;

3.

  • Responsiveness to NRC initiatives;

4.

Enforcement hi story;

5.

Operational events (including response to, analyses of, reporting

of, and corrective actions for);

6.

Staffing (including management); and

7.

Effectiveness of training and qualification program.

However, the NRC is not limited to these criteria and others may have

been used where appropriate.

On the basis of the NRC assessment, each functional area evaluated is

rated according to three performance categories.

The definitions of

these performanc~ categories are as follows:

Category 1:

Licensee management attention *and involvement are readily

evident and place emphasis on superior performance of nuclear safety or

safeguards activities, with the resulting performance substantially

exceeding regulatory requirements.

Licensee resources are ample and

effectively used so that a high level of plant and personnel performance

is b~ing achieved.

Reduced NRC attention may be appropriate. *

Category 2:

Licensee management attention to and involvement in the

performance of nuclear safety or safeguards activities are good.

The

licensee has attained a level .of performance above that needed to meet

regulatory requirements.

Licensee resources are adequate and reasonably

allocated so that good plant and personnel performance is' being

achjeved.

NRC attention may be maintained at normal levels.

Category 3:

Licensee management attentibn to and involvement in the

performance of nuclear safety or safeguards activities* .are not

s~fficient. The lic~nsee's perform~nce does not s~gnificantly exceed

that needed to meet minimal regulatory re~ui r.~ments~ *_Licensee resources

appear to be* strained or not e(fectively ~ied.

NRC ~tt~ntion should be

increased above normal levels.

-

-- ------

--

--~---

3

.. -

The SALP Report may include an appraisal of the performance trend in a

functional area for use as a predictive indicator.

Licensee performance

during the assessment period should be examined to determine whether a

trend exists.

Normally, this performance trerid should only be used if

a definite.trend is discernable.

The trend, if used, is defined as:

Improving:

Licensee performance was determined to be improving during

the assessment period.

Declining:

Licensee performance was determined to be declining during

the assessment period, and the licensee had not taken meaningful steps to

address this pattern.

4

IV.

Performance Analysis

A.

Plant Operations

1.

Analysis

Evaluation of this functional area was based on the results of

routine inspections by *the resident inspectors, one Augmented

Inspection Team (AIT) inspection, and one rciutine fire

protection inspection.

Enforcement history in this functional area improved since the

last SALP rating with only t~o violations (1 Severity Level IV;

1 Severity Level V).

One of the violations pertained to a

failure to follow procedures during a ground checking evolution

which resulted. in a reactor scram.

This violation occurred

early in the assessment period and effective corrective actions

prevented recurrence.

The second violation pertained to an

iMadequate operational procedure.

Although this violation was

issued during this period, the event occurred during the

previous assessment and does not reflect performance in this*

peri~d.

The corrective actions were effective in preventing

recurrence.

The licensee requested and received one waiver of

complianc~ pertaining to the testing of the reactor protection

system (RPS) electrical protection assemblies on Unit 3.

The

request was well prepared~ accurate and timely.

The licensee

also submitted a request to revise the Technical Specifications

to eliminate any further requests .for discretionary action on

this issue.

Licensee events attributed to personnel errors continu~d to

d~crease. One reportable event associated with pla~t

operatio~s involved personnel error.

This event involved a*

reactor scram as discussed previously, and occurred during

the first m6nth of the assessment period~ The corrective

actions were effective in preventing recurrence of both

personnel ~rrors and scra~s associated with plant operations.

The Dresden plant showed an improved trend in its operating

p~rformance during this period.

Although eight scrams occurred

early in the assessment period, both units were operated for

long continuotis periods.

Unit 3 exceeded its previous record

for continuous days on line.

Seven of these scrams were a

result of equipment failures and surveillance activities and

are discussed in Section IV.C.

Engineered safety features

(ESF) actuations we~e low with improvement in ESF actuations

attributable to outage testing.

During the previous assessment,

the 12 ESF actuations that occurred during outage testing.were

identified as a weakness .. During the recent Unit 3 outage

only three ESF actuations occurred.

One safety injection also

occurred as the result of a false signal being generated by a

leaking test isolation valve.

. .

The operating-department demonstrat~d ~ood superv1s1on and

coritrol of plant activities and excellent response to off-normal

5

events.

Examples included two loss-of-offsite-power events,

a feedwater transient, and reactor scrams.

The operator

actions durjng the feedwater transient rapidly mitigated the

transient and ptevented a reactor scram.

During these events,

the operators' actions were effective in mitigating the plant

upset conditions and demonstrated both effective training and

a conservative approach to safety .. The operating crews

displayed a high degree of attentiveness, were knowledgeable

of plant status and regulatory requirements, and projected a

positive safety attitude.

Control rotim conduct was professional

and businesslike.

Operating personnel demonstrated good

procedure discipline and effective use of plant drawings and

task briefings.

Aggressive management and supervision

immediately detected and 2orrected pos~ibilities for errors

during implementation before they became actual problems.

Examples of these possible errors included procedure adherence;

and removing equipment and 1nstruments out of service.

The

corrective actions addressing these cases were prompt and

effective, resulting in improved attentiveness.

The operati~g staff interface with NRC was open and candid.

This was evident in their communication of problem identification.

and resolution, by the operating staff's responsiveness to NRC

observatio~s,.and with NRC management during site visits.

The overall appearance of the control room improved significantly

ctimpared to the previous assessments.

These improvements were

due to modifications made as a result of detailed control room

design review (DCRDR) requirements, but also are attributable

to continuing hardware and environmental changes proposed by

the operations staff:

Housekeeping conditions within the plant were very good

throughout the assessment period, including refueling outages:

Management was aggressively involved in the assurance of

quality in plant operations and demonstrated support of*

improvement initiatives. Oil and water leaks were identified

and repaired.

The number of existing leaks was previously

identified as a weakness.

Other improvement initiatives

included the ~ystem labeling, valve tagging and breaker cubicle

identification programs.

These programs were effective in

preventing identification errors and inadvertent manipulation

of components on the wrong unit.

Continued improvements in

the effective cooperation between management and the operating

staff were also noted.

For example, management performed

frequent in-plant self-assessments aod. held aggressive onsite

root cause determi~atiorr critiques involving all plant

departments.* These critiques were effective in determining

subsequent corrective actions.

The previous SALP assessment identified that teamwork between

the various departments had improved at Dresden in regard to

addressing some of the more significant pr,oblems.

The

implementation and expansion of this conce~t continued.

Examples included the assistance from the operations department

6

..

in identifying problems with 4-kV breakers; cooperation with

the instrumentation department in dev~loping and obtaining

improved reactor process instrumentation in the control room;

combined efforts of all departments during the preventive

replacement of a main transformer and the reactive replacement

of the failed reserve auxiliary transformer; and the assistance

of operations in the development of good target analysis and

planning in preparation for the NRC Regulatory Effectiveness

Review.

Other demonstrations of effective teamwork were the

good housekeeping conditions during outages and the revision

of the emergency operating procedures (EOPs).

The EOPs,

previously. identified as a weakness, were found to be above

average.

The control and overview of outage-related activities by the

operating staff resulted in reduction of ESF actuations,

reduction of system lineup and verification errors~ and the

overall good housekeeping conditions during the outage.

Previous SALP assessments identified outage contror as a

~eakness* because of the high occurrence of ESF actuations.

Although the cu.rr.ent licensed staff performed we 11 during

events, because of effective training, the recent initial

senior reactor operator (~RO) and reactor operator (RO)

examinations indicated weaknesses in. training as discussed

in Section IV.F.

One of three (33%) senior reactor operators

and two of *five (40%) reactor.operators failed the examination

  • for a total failure rate of 37.5 percent.

Staffing for plant operations was very good and the licensee

effectively* trended and controlled operator overtime.

The

operations staffing includes four senior reactor operator and

four reactor operator licensed individuals per shift for six

shifts. Additionally, a complete extra shift of four SROs is

maintained to assist in shift manning and improvement initiatives.

The initiation of the fourth reactor operator in th~ control

room wa~ effective in providing an additional trai~ed operator

to assist in mitigating off normal conditions and during high

activity periods.

Additionally, improvements in the fire

protection program resulted with the addition of an~ssistant

fire marshal.

2.

Performance Rating

The licensee's performance is rated Category 1 i.n this area.

The licensee's performance was rated Category 1 in the previous

assessment period.

3.

Recommendations

None.

7

B.

Radfological Controls

1.

Analysis

Evaluation of this functional area was based on the results of

seven inspections conducted by regional inspectors and observations

made by the resident inspectors.*

Enforcement history during this assessment period was good with

one Severity Level IV violation issued.

Staffing, traihing and qualifications were adequate during the

assessment period, with chemistry stronger than radiation

protection.

The as-low~as-reasonably achievable (ALARA) staff

was weak and had significant turnover during the middle of the

period, but was re-staffed with individuals with extensive and

appropriate nuclear power plant experience.

Two degreed .individuals

were added to.the radiation protection staff as replacements;

however, neither had nuclear power experience.

In chemistry,*

prof~ssional staff experience levels ha~e improved and are

generally good .. The permanent assignment of technicians, all

American National Standards Institute (ANSI) qualified, to

chemistry has substantially improved laboratory capabilities and

  • technician proficiency.

Management involvement in ensuring quality was adequate .

Management attention was not sufficient*to ensure that c_orrective

actions for problems identified and documented in radiological

occurrence reports (e.g., contamination and high radiation area

controls) are sufficient to prevent recurrence.

In addition,

problems involving inadvertent disposal of a batch waste release

tank composite sample, incorrect verifications of liquid effluent

monitor setpoints, untimely correction of airborne radioactivity

releases from the hydrogen addition system, and inadvertent

release of contaminated scaffolding from the site highlight the

need for greater management involvement.

The water chemistry

program conformed to the Electric Power Research Institute

(EPRI) boiling water reactor (BWR) owners Chemistry Guidelines

and was under good control, as demonstrated by parameter trend

charts.

Hydrogen water chemistry on Unit. 2 to reduce intergranular

stress corrosion ~racking (IGSCC) has improved the overall water

chemistry, however, a new electrochemical potential monitor

install~d to optimize hydrogen *addition (and therefore not

unnecessarily inc~eas~ radiation levels) is not yet operational.

Laboratory facilities were greatly improved and analytical

instrumentation was extensively upgraded:

Respon~iveness to identified concerns was generally good.

The

licensee has been receptive to the confirmatory measurements

programs and has improved both the radiological and nonradiological

laboratory quality assurance/quality control p_rograms.

Detailed

discussions were held regarding the status:of several highly

~

.

-

-

8

  • -

contaminated radwaste rooms and the licen~ee initiated corrective

action to decontaminate these rooms.

However, the licensee has

a number of unattended exits from the radiologically controlled

area which increases the potential for contamination control

degradation. *Also, the amount of contaminated dirt, shielding,.

and other material ~tared onsite remains hig~.

The licensee 1 s approach to identifying and resolving technical

issues was adequate.

Implementation of.radiological controls

was good during and after the release of radioactive isotopes

contained in water vapor from the Unit 2 isolation condenser

(IC) on March 25,

1989~ The licensee has since developed a .

method o( feeding clean ~ater to the shell side of !Cs when

offsite power is lost; this develo~ment corrects a long-standing

radiological problem that occurred when offsite power was lost

during power operations.

The total station dose .for 1989 ~as

1139 man-rem.

This total is understandable given the

contribuiion from two refueling outages. and a major project to

upgrade radwaste facilities. *In 1988, the total station dose

was 1407 man-rem.

The licensee also significantly reduced the

number of personal contamination events, from 534 in.1988 to 215

in 1989, which is indicative of improving performance .. This

reduction has been achieved through in~reased worker training,

plant material condition improvements, and greater management*

review of contamination e~ents. However,

s~ve~al recent

whole-body exposures in excess of administrative limits and. a

. 7 rem extremity exposur,e that was significantly higher than

projected, indicate a continuing weak~ess in pre-job dose

evaluations.

No unplanned liquid or transportation incidents

were reported during the assessment period.

Gaseous-activity

r:.eleased was very low.

Liquid activity released and volume of

solid radwaste w~re average.

The results of the nonradiological confirmatory measurements

program were good.

With 26 of 30 initial analyses in agreement

.and two qualified agreements, the quality of measurement improved

from that in the previous period.

The results of the radiological*

confirmatory measurements were adequate with five disagreements

in 30 comparisons m~de on six routinely used samples on.three

detection systems.

The Radiological Environmental Monitoring

. Program operated satisfacto~ily.

2,

Performance Rating

The licensee 1s performance is rated Category 2 in this area.

The licenseeis performance was rated Category 2 in the previou.s

~ssessmeMt period.

3.

Recommendations

None.

9.

-*

  • - ,-- " ---

-

C.

Maintenance/Surveillance

1.

Analysis

Evaluation of this functional area was based on routine and

special inspections, and a maintenance team followup inspection,

by the resident and regional inspectors, including two AITs.

The enforcement history in thi's functional area showed improvement

with three Severity Level IV and one Severity Level V violations

compared to five Severity Level IV and one Severity Level V

violations during the previous assessment period.

Two of these

violations concerned maintenance activities while the other

related to surveillance activities.

One involved inadequate

maintenance and post-maintenance testing regarding control rod

charging water check valves prior to )986 and the other concerned

a failure to pl ace an emergency core cooling system ( ECCS)

initiation level switch in the proper tripped condition during

maintenance.

The third violation involved_placing the service

air system containment isolation valves in a test condition

without use of a procedure during an integrated leak rate test

(ILRT).

There was no improvement in the total number of component

failures reported in li~ensee event reports (LERs) and reactor

scram events during this period. Thirty-five of the 50 LERs were

attributable to the Maintenance/Surveillance functional area

co~pared with 21 of the 41 LERs d~ri~g the previous period. *

Twenty of these LERs were attributable to component/equipment

failures as opposed to other root causes.

There were two LERs

associated with personnel errors, indicating good personnel

performance practices.

Seven of ~he eight reactor scrams were

attributable to component failur~s-compared to the previous

period when one scram occurred.

However, four cif these scra~s

were the result of initiators that were either spurious or from

offsite equipment failures.

These included the March 25, 1989

loss of off site. power from a failed 345 kV switchyard circuit*

breaker; the March 30, 1989 spurious reactor protection system

(RPS) electrical protection assembly (EPA) breaker trip durtng

surveillance testing; the July 12, 1989 spurious main steam

isolation during surveillance testing; and the January 16, 1990

failure of a condensate pump motor from an undetectable internal

fault.

Two of the scrams resulted from noise occurring during

RPS surveillance testing at power.

One of the licensee's

proposed corrective actions is to perform this surveillance

during shutdown conditions.

This proposal is currently unde~

NRC review.

None of the scrams were directly related to an

ongoing maintenance activity and only one of the scrams was

directly related to the actual methodology of a surveillance

activity conducted at the time of the scrams.

The January 5, 1990

scram during the main steam line high .flow surveillance was

attributable to an inadequate venting proced~re.

10

Management's involvement to ensure q~ality in maintenance and

surveillance activities was effective as demonstrated by prior

planning and assignment of priorities, policies being well

stated and disseminated, decision making usually at a level that

ensured adequate management review, corpor~te management involvement

th~t was effective in assuring iompletion of improvement goal.s

and root cause analyses that usually resulted in. improvements.

The licensee was effective in assuring that scheduled surveillances

were completed.

No surveillances were missed during this

assessment.

Supervisory tours of the plant increased and

communications improved between maintenance and* supporting

groups.

Implementation of a very extensive Maintenance Improvement

Program (MIP) continued from the previous period.

This program

r~sulted in cont~nued good performance of the diesel generators

and high pressure coolant injection (HPCI), and in the improved

a~ailability of the low pressure injection systems.

The

effectiveness of the motor operated valve improvement program

resulted in significant reduction of valve f~ilures from 12 in

1987 to 8 in 1988 and 2 in 1989.

Managemeht 1 s fnvolvement in

the security preventive maintenance program resulted in significant

reduction in corrective work activities.

Management overview .

also resulted in the completion of the recent Unit 3 refueling.

outage on schedule with minimal problems.

A detailed planning

program was incorporated that effectively set the prior{ties *

and scheduling of these tasks to ensure use of a 1,1 resources.

The licensee also implemented a program to effectively prepare

for maintenance activities during unexpected outages.

The

operating staff in cooperation with the maintenance staff

maintained prepared corrective work requests to b~ performed

~uring short outages.

Thes~*preparations allowed the licensee

to effectively resolve most of the degraded equipment that would

normally only be ~ddressed during the scheduled outages.

Departmental effectiveness was enhanced through improved

.

. communications, meetings between all departments, and detailed

coordination of activities.

Conversely, because the Maintenance Improvement Program for**

balance of plant equipment (BOP)_ is not scheduled for completion

unti.l 1992, not all of the goals were achieved.

Many of the BOP

equipment programs were not fully implemented and, as.such, were

not y;.1.t effective.

This was evidenced by the January 16, 1990

scram and loss of offsite power event.

Although the reliability

of safety-related equipment has improved, th.e reliability of BOP

equipment did not improve as evidenced by_the number of component

failures.

The preventive maintenance (PM) program continued to improve in

certain respects but some specific weaknesses were still evident

with procedures, and problem analysis data sheet control.

Also,

there was an indication of a lack of PM on a shutdown cooling

pump outlet valve that failed due to a sheare.d shaft key .. In

the first half of the assessment period,.the scope of the PM

11

'program was incomplete and PM was ineffective as evidenced by

the lack of scheduled maintenance on 250 VDC HPCI motor control

centers, safety-related and BOP 4.16 kV breakers and the larger

number of potentially significant ~vents in the first quarter of

1989.

However, aggressive management involvement resulted in

considerable improvement in the latter half of the period

specifically in the electrical area, the check valve inspection

program, control room instrumentation, and the BOP motor 6perated

valve overhaul program.

The improvements were also attributed

to attention to detail and pride of workmanship by maintenance

and support personnel.

Increased emphasis on predictive maintenance

techniques was demonstrated by the pre-failure replacement of

the Unit 3 main transformer.

Additional predictive techniques

of equipment failure were being developed by the licensee such

as a thermography program.

Detection of intergranular stress

corrosion cracking (IGSCC) of piping was improved with surface

enhancement of the inspected welds. The licensee plans to

prepare all IGSCC susceptible welds for future inspections.

The, licensee's approach to resolving technical issues from *a

safety standpoint was sound and thoro~gh. A clear understanding

of these issues was demonstrated by management through discussions

with NRC.

Conservatism was generally exhibited when the potential

for safety significance existed.

The licensee's in-service

testing program was considered effective as demonstrated by the

high availability of ~otor operated valves.

Conser~atism with

respect to safety was exhibited by declaring pumps and valves

inoperable when discovered rather than at the conclu~ion of

testing.

Licensee augmented inspections were implemented to

assure that degradation of safety-related components was monitored

arid contro 11 ed.

Conversely, the frequency *of a chi evi ng an

annunciator

11blackboard

11 status declined during the first half

of this assessment period; however, improvements were made late .

in the assessment period with assistance -0f the operations

department to return annunciator status to similar conditions of

_the previous period.

Corrective actions described in LERs were generally ad~quate,

but not all of the corrective actions were completed in a timel~

manner.

Some of these corrective actions did not prevent

.

recurrence:

Although they met the regulatory requirements, the

licensee could have done more to reduce the leakage rate from

cont~inment isolation valves during the Unit 3 refueling outage.

The failure to vent the service air system during the Unit 3

ILRT also indicated an inadequate licensee evaluation of this

activity. This problem was attributable to weaknesses in staff

kn owl edge.

..

Licensee management was responsive to NRC initiatives, as

evidenced by their prompt actions to Information Notice (IN) 90-02,

11 Potential Degradation of Secondary Containment 11 by

-comp 1 et i ng a tho:roughwa 1 kdown and maintenance review. of the

--


  • - ----

12

ventilation and standby gas treatment systems.

The licensee's

maintenance activities related to this IN, and application of

"lessons learned" in IN 90-11, Maintenance Deficiency Associated

With Solenoid Operated Valves, and Bulletin 89-02, Stress

Corrosion Cracking of High-Hardness Type 410 Stainless Steel

Internal Preloaded Bolting in Anchor Darling Model S350W Swing

Check Valves or Valves of Similar Design, were very prompt and

effective.

In the case of IN 90-11, although the type of

solenoid mentioned in the notice was not used at Dresden, the

licensee applied the guidance to the specific solenoids that

were utilized ~t Dresden.

Responses and actions were adequate

to assure the potential maintenance related discrepancies

addressed by Generic Letters were inspected, evaluated and

corrective action taken when required;

Additionally, the

licensee was prompt in correcting deficiencies associated with 4

kV breaker preventive maintenance.

When the NRC raised concerns

relating to maintenance or surveillance activities, the licensee

usually responded in a timely and effective manner.

Communications

between the licensee and the NRC were generally good.

Staffing in the maintenance/surveillanc~ area was adequate.

Additional personnel were added to the Maintenance Improvement

Program during this asse~sment period to aid in implementation

of the programs and the. upgrade of the maintenance procedures.

The corrective maintenance backlog was not excessive with

about 850 work requests (corporate goal is 900) for the available

resources.

Staffing was augmented by contractor's for specific

activitie~ s~ch as. non-destructive examinations (NOE).

The

licensee also used the servi~es of CECo System Materials Analysis

O~~artment (SMAD) for consultation on NOE verification and

corporate staff to augment limited plant staff expeftise regarding

leak rate testing.

Maintenance department personnel training and qualification

programs were acceptable and improving.

Personnei received the

required training under the accredited program for performance

of their assigned duties.

  • *

Personnel involved in the supervision of assigned ta~ks appeared

to be well trained and knowledgeable of task objectives as

~vident in the reduction of maintenance related errors during

outages.

This was identified as a.weakness during the previous

assessment.

Training and qualification of inservice testing

personnel and of NOE inspection contractors was adequate.

2.

Performance Rat~ng

The licensee's performance is rated Category 2 in this area.

The licensee's performance was rated Category 2 in the previous

assessment period.

13

3.

Recommendations

None.

D.

Emergency Preparedness

1.

Analysis

Evaluation of this functional area was based on one routine

  • inspection, two annual e~ergency preparedness (EP) exercise*

inspections, one special inspection of corporate support activities

of EP, and a special Augmented Inspection Team (AIT) inspection.

Enforcement history_ has remained good.

No violations were

identified during this or the previoui assessment period~

Management involvement in assuring quality continues to be good.

Fouf quality assurance (QA) audits were completed during this

assessment period.

Two assessed onsite activities, one focused *

on offsite matters and one concerned corporate emergency

preparedness issues.

Several QA surveillances of EP activities.

were also conducted.

Where necessary corrective actions have

been initiated or completed to address items found through these

self a~sessments.

The licensee'~ response.to operaiional eventi was good.

Seven

emergency p1an activations occurred in this assessment period.

Each event was correctly classified in a timely manner.* Six

events were classified as Notifications of an Unusual Event and

one as an Alert. Appropriate notifications to the State, counties

and the NRC were made ~ithin th~ required time limits for each

event.

The li2ensee effectively utilized the emergency response

facilities, procedures and organization to evaluate plant c

conditions and anticipated actions to successfully mitigate the

consequences of an event which occurred jn*March 1989 which did

not procedurally requir~ that l~vel of response.

Responsiveness.to identified concerns was good.

An exercise

weakness for failure to provide adequate contamination and

exposure control was identified during the evaluat.ion of the

April 1990 annual exercise.

In response to the exercise weakness,

licensee management promptly scheduled * drill to.demonstrate

contamiriation and exposure control.* Additionally, recommendations

for improvement have been appropriately evaluated and considered

by licensee personnel .

The licensee's identification and resolution of technical issues

has been excellent.

During this assessment period the entire

vol~me of Emergency Pl~n Implementing Procedures (EPIPs)-were

reviewed and revised.

Many EPIPs were shortened and provided

with checklist aids to improve ease of~use. In response to the

em~rgency plan activations the licensee tond~cted post-activation

14

reviews for each event to identify areas which could be improved

upon.

Items identified through these reviews of real events

,

have been incorporated into the licensee's Nuclear Tracking

System and appropriately resolved.

Staffing l~vels for the Emergency Response Organization (ERO)

remain good.

Semiannual off-hours drills have been conducted

to demonstrate the capability to augment onshift personnel in a

  • timely manner.

The EP staff has increased during this assessment

period to include a Lead EP Coordinator and an EP Coordinator.

There is also a training staff member assigned responsibility

  • for.EP training.

The Lead EP Coordinator reports directly to

the Technical Superintendent, who in turn reports to the Station

Manager, ensuring EP concerns receive ready access to upper

management.

The licensee's EP training program was ex~ellent. In addition

to the required annual retraining, all members of the ERO were

provided additional training on the revised EPIPs.

Training

records were meticulously maintained and an appropriate training

matrix established and implemented.

A new training module was

developed to strengthen a weakness that had been identified with

Operational Support Center personnel's knowledge of emergency

response activities.

The training program's effectiveness is

evidenced by the licensee's generally good response during.

emergency exercises.

The scenario's prepared for the exercises

were sufficiently challenging to test the licensee's emergency

response capabilities.

During the exercises the licensee made

extensive efforts to use mock-ups to provide realistic conditions

.for the emergency responders.* The complexity of the responses

necessary to suppor*t the use of mock-ups in the exercises po.sed

new challenges to the licensee's exercise control organization.

2.

Performance Rating

The licensee's performance is rated Category 1 in this area.

The licensee's performance was rated Category 1 during the

previous assessment period.

3:.

Recommendations

None.

E.

Security

1.

Analysis

Evaluation of this functional area was based on the results of

three routine inspections conducted by regional inspectors and

observations made by resident inspectors.

Additionally, a

Regulatory Effectiveness Review (RER) was. conducted.

15

Enforcement related performance has essentially remained the

same~ Three violatio~s (2 Severity Level IVs; 1 Severity Level

V) were identified during this period compared to two during the.

previous assessment period.

Reportabl~ security events were properly identified and analyzed.

The licensee had two reportable security events during "the

~ssessment period, neither resulted in violations.

During the

  • latter part of this assessment period, a significant increase in

the number of loggable security events was noted.

This increase

  • was largely a result of expanded and revised corporate guidelines

which were developed in response to NRC concerns noted during

the previous SALP assessment period. *The scope of the licensee's

procedures for loggable items now more closely follows regulatory

guidance.

The majority of loggable events identified particular*

problems with environmental effects related to the closed

circuit television system and perimeter alarm system.

Because

these expanded data became avaiJable only near* the end of the

assessment period, the NRC staff .is still analyzing them.

Management involvement in assuring quality was good and is a*

program strength.

This was evidenced by the licensee's planning

and ~mple~entation of a restoration project w~ich has significantly

increased th~ effectiveness of the protected area b~rrier and

.associated alarm system.

The license~ also develo~ed and

implemented an equipment upgrade. that. significantly incr:-eased

their aisessment capability of the protected area perimeter.

In

addition, the licensee has expanded its use of contract security

personnel to conduct audits/survei l lan*ces of the security .

  • .
  • prog_ram.

The licensee's approach to the identification and resolution of

technical security issues was *excellent and ~s a program strength.

This was evidenced by the licensee's continuing implementation -

of its performance indicator prog~am and mana~ement's involvement

in root cause analysis of identified concerns.

Also management

has taken an aggressive approach.to resolve issues that are

identified through event logs.

Initial rev.iew showed effective.

licensee planning to identify causes and actions needed to

r~solve the problems.

Responsiveness to identified problems is good and corrective

actions are comprehensive and completed in a timely manner.

However, on one occasion during this assessment period, corporate

security arid licensing failed to adequately monitor licensee .

commitments to the NRC which resulted in the licensee's failure

to implement corrective action in'a timely manner.

This failure

to mbnitor ~nd implement corrective action commitments resulted

in Dresden receiving a violation for the same type of event that

was previously identified at ano~he~ Commonwealth Edison site~

Communications with regional safeguards:personnel continues to

be frequent and effective and is a streng~h of the program:

16

  • ,

2.

.

.

.

.

Staffing has been expanded during this assessment.perio.d and is

ample.

The licensee has increased their utilization of the

contract se6urity organization.

The contractor's staff has been

given increased responsibility by the licensee in the collection,

analyzing and dissemination of security data to the licensee *

relating to the effectiveness of security equipment and performance

of security force personnel.

To accomplish this task the senior.

management level. of the contract security force has been increased

in size.

This expansion has enhanced the proactiveness of the

security program through the early identification and correction

of potential problems.

The licensee's security force was adequately supervised and

  • trained.

Generally, the licensee's procedural guidance for the

security force was sufficiently detai]ed to ensure that personnel

are knowledgeable of their responsibilities and conduct their

duties in an effective manner.

The training and qualification

program utilized by the licensee and implementation by the

security contractor was considered acceptab 1 e and meets, commitments.

However, the tactical contingency training program recently '

developed and implemented by the licensee/security contractor

exceeds commitme~ts and is a program strength.

The RER concluded that the licensee's security program had many

strengths and it. was evident that the ~licensee had commi.tted

expanded resources to improve its security program.

The RER

identifi~d no major problems but did identify° several areas in

.the licensee's program that could.be strengthened or improved.

The licensee has acted in a positive and aggressive manner to

implement improvements.

Performance Rating

The.licensee's performance is rated Category 1 in this area.

  • The licensee's performance was rated Category 2 improving during

the previous assessment period.

3.

Recommendations

None .

. F.

Engineering/Technical Support

1.

Analysis

Evaluation of this functional area was based on the results of

three routine, one special, and two team inspections by regional

inspectors; inspections by the resident -inspector; and interactions

with the licensee and review of licensee submittals by the

Office of Nuclear Reactor Regulation {NRR) staff.

17.

One Severity Level IV violation was issued during this assessment

period.

The violation invol~ed the licensee's failure td

control the design of a fire penetration in a 3-hour fire rated

wall. While this violation had no major safety significance,

when taken in combination with other events in which maintenance

personnel failed to recognize a fire barrier, it reflects a

weakness in the licensee's implementation of its fire protection

program ..

Ten licensee event reports (LERs) were attributed to this area.

Six were the result of design problems of which only one (caused

by a loose wire connection to a thermal overload due to an

incorrect tightening criteria) was attributed to activiti.es

performed during this assessment period.

The other design

problems w~re related to design activiti~s performed during

previous assessment periods or original plant design deficiencies.

Three were related to inadequate procedures; and one ~as due to *

personnel error (improper inspection of a fire penetration

device).

None of the events appeared to be indicative of

programmatic weaknesses.

Management involvement to assure quality continued to be mixed.

On the positive side, the licensee has improved its performance

in the a~ea of design changes, especially on post-modification

. testing.

Identification and tracking of the Top Technical

Issues ensured man~gement and engineering attention toward

specific and difficult :to rectify technical issue*s such as the

main

~team line temperature switch drifting and reactor/turbine

building ventiiatio~ problems.

Management involvement in

ensuring comprehensive corrective actions for deviation reports

was evident.

Management also ensured that offsite engineering

resources were effectively utilized.

Safety evaluations continued

to have a sound engineering basis, and t~mporary modifications

were few in number and well controlled.

In fire protection, the

licensee has shown a willingness *to test equipment, develop

preventive maintenance for fire prot~ction equipment, and

develop fire plans for areas not covered by the Fire Hazards

An~lysis report, such as the hydrogen storage areas.

On the

negative side, at the beginning of the assessment period, a

walkdown and physical inspection of ,equipment required to be

  • environmentally qualified (EQ) was performed which found several

terminat boxes and one terminal block' which failed to meet EQ

requirements; subsequent to the end of the assessment period,*

additional problems in the identification and qualification

of EQ equipment were identified.

Another area not receiving

adequate management attention has been the performance of the

condensate/condensate booster pumps.

While not safety-related,

these pumps have continued to cause loss of reactor feedwater

transients and resultarit reactor scrams despite several

modifications performed since 1987 to the auto-start logic.

In

addition, several initial licensing*submi~tals were incomplete

18

by not providing all of the technical information used by the

engineering evaluations, necessitating additional request~

for information to complete the reviews.

Other weaknesses identified late i~ the assessment period

included the numerous deficiencies in the material supplied for

the initial licensed operator examiriations.

The facility

pre-examination review did not appear to resolve examination

inaccuracies as evidenced by the number of post examination

comments.

In addition, the examination results showed a weakening

in the effectiveness of the licensed operator training program

for new operators with regard to administrative procedures,

familiarity with routine shift administrative duties, EDP

implementation, and lack of proficiency in the use of the

Generating Stations Emergency Plan.

The EDP followup inspection

found that the revised EOPs were significantly improved over the

earlier versions with regard to clarity and ease of use.

Two

weaknesses were identified however, one that related to the lack

of a basis document that could provide justification for differences

between the plant specific technical guidelines and the EDP flow

charts and another regarding the lack*of documentation that

provided justification for the programmatic changes to the EDPs.

The licensee's approach to the identification and resolution of

technical issues was good.

In the temporary modification*

program, there was clear understanding of the us~ of temporary

  • measures to resolve technical problems.

The temporary modifications

were few in number, had definite scop~s, thorough evaluations~

and defined permanent resolutions.

The licensee self-identified

past design problems such as the low pressure coolant injection

(LPCI) swing bus, s_tandby gas treatment system (SGTS), and

atmospheric containment atmosphere dilution/cont~inment atmosphere

monitor power supply design discrepancies, single recirculation

loop stress analysis deficiencies, an_d design basis accident

analysis discrepancies in regard to consideration of swing bus

transfer time.

This commitment to self-identification was also

evident through a system engiheer who identified a*self-made

error that had caused a missed Dresden administrative technical

requirement.

The engineering and safety evaluations *prepared

for modifications were thorough And technic*lly sound.

Although

processing delays of problem analysis data sheets existed, those

that were processed were adequate.* Although also at ti.mes

delayed, responses to deviation reports were thorough and

reflected a conservative approach to safety.

Most engineering

work for modifications was completed well in advance of the

planned implementation.

The staffing of the onsite engineering and technical support

groups was insufficient with respect to the work load during

this assessment period.

This was demonstrated by delays in

problem analysis data sheet and deviation report preparation.

Competition of various activities for tec*hnical staff engineer

19

availability was eveTI more pronounced during the Unit 3 refueling

outage.

The licensee recognized this problem and addressed it

with staffing increases throughout the assessment period and

planned additional staffing increases to further address the

problem.

The system engineer staff included positions and responsibilities

that were clearly defined.

The licensee was in a transition

phase; so that while expertise was generally available, it was

not always with the person who had the assigned responsibility.

Th~ LPCI injection val~e stem to plunger separation event

indicated inadequate involvement of technical staff engineers in

immediate problem analysis.

In addition, inadequate system

engineer knowledge in regard to analysis of motor operated valve

test data was evident.

The licensee recognized these weaknesses.

and was attempting to rectify them by providing additional motor

operated valve tr~ining. The licensee also implemented expanded

general systems training for systems enginee~s.

In general, training of non-licensed operators appeared adequate.

Initructors were knowledgeable of their subject area, and

considerable positive feedback was obtained from participants .

. 2.

Performance Rating

The 1icensee*s:performance is rated Category 2 *in this area.

The licensee 1 s performance was rated Category 2 dudng the

previous as~essment period:

3.

Recommendations

None.

G.

Safety Assessment/Quality Verification

1.. *Analysis

Evaluation of this functional area was based on the results of

routine and special inspections, including two AITs, by the

resident and regi~na1 inspectors.

In addition, NRC staff review

of licensee submittals and requests.for amendments to the

operating license was considered.

Enforcement history in this functional area was good with only

one Severity Level V violation.

This violation involved a*

failure to perform an adequate i ndepe_ndent verification.

The

licensee took prompt and effective corrective actions as evidenced

by lack of recurrence .

20

Management's involvement in ensuring quality. was generally good.

Management exhibited good performance in regard to the quality

verification self assessments, as demonstrated by the reduction

in the number of LERs attributed to personnel errors, good plant

housekeeping, and improvement in the station's performance

during non-routine activities such as outages and the return to

service following outages.

Several major audits were conducted

.of the radiation protection area.

The audits were in-depth with

a good mix of programmatic and performance-based review of

activities.

In addition, radiation protection management

participated in audits at other nuclear power plants.

Implementation of the Dresden Station Improvement Plan (DSIP)

continued from the. previous assessment period including changes

near the end of the p~riod to ihift overall responsibility for.

the program to a more in-line function.

These changes were ~ade

as a natural -evolution of the program to place more reliance on

an organizational culture committed to safety and quality

improvements .. A number of beneficial programs evolved from*

or were affected by the DSIP, such as the MIP, Scram/ESF Actuation

Reduction Program and the Top Technical Issues.

The Top Technical

Issues program is a management tool to track and plan resolution

of various eng~neering issues such as improved performance of

systems, components, and overall plant performance.

Various

issues, such .as; drywell cooling, feedwater regulating valve

modifi~ations, and feedwater heat~r leakage were tracked through

~esolution with the Top Technical Issues Report.

The report

maintains a current history of the issue, engineering evaluations,

and ma~agement analysis.

The status of corrective action

  • completion is described and maintained current.

Additionally,

  • .the daily unit operating performance report, a 1 so prepared by

the technical staff, is used by management to monitor the plant

performance through parameters for various safety and balance of

plant systems, including drywell temperature, recirculation pump

seal temperature and pressure, and feedwater heater drain

temperaturas.

Although still in the implementation phase, the

MIP was utilized in addressing numerous internal and external

mainten~nce ~ffectiveness concerns as described in the

Maintenance/Surveillance section of this report:

The Scram/ESF

Actuation Reduction Program was regarded as an excellent program

to determine root cause and to implement corrective actions

to reduce adverse events.

Most notable was the inclusion of

near misses (half scrams and half isolations) for Scram/ESF

actuation investigation thresholds. The increase in the number

of scrams in this assessment period compared to the previous

period did not r.eflect licensee initiatives in this area, in

that, the licensee extensively addressed each to prevent

recurrence.

Corporate management was frequently and effectively involved in.

site activities as evidenced by critical self:-*assessments

performed by corporate personnel, the BWR General Manager's

21

attendance at the Unit 3 post-refueling outage startup onsite

review meeting, and the rec~nt assignment of a plant specific

cognizant individual from the Vice President-BWR Operations

staff to ensure.corp6rate management awareness of plant activities

- and status.

Management involvement and concern for Technical

Specification compliance was exhibited by *conservative Technical

Specification shutdown decisions involving a failed recirculation

pump seal, a drywell personnel interlock local lea~ rate test

( LLRT) failure, and .HPCI structura 1 support damage.

Management remained well informed and aware of internal plant

activities and* applicable activities at other plants.

Frequent

plant tours by manage.ment encouraged improved cleanliness/

housek~eping conditions ~nd the identification and tracking of

water and oil leaks for repair .. An example of these findings

included the identification of a degraded fire barrier by the

  • plant manager.

The monthly status reports evolved into an

excellent management tool for re_maining cognizant and identifying

trends in various departmental indicators.

A riotable exception,

however, was the absence of indic~tors to easily monitor the

effectiveness of the MIP.

-

-

Monthly performance review meetings encouraged non-supervisory"

.

representative participation such ~s to elevate concerhs* to a

higher management level.

These meetings also usually included a

repr~sentative from the Quad Cities plant to extend the ~haring

of experiences._ This .same goal was also addressed by.discussion

of. other CECo plant events during the daily morning meetings.

The.QA-superinte~dents meeting held at Dresden encouraged the

effective transfer of information and included a tour of the

facility and subsequent discussion of observations.

Specific_*

examples of in.corporation of experiences observed at other.

plants included the discovery of pathways not addressed in the

LLRT pro~ram, design basis accident analysis deficiencies, area -

combustible material loading deficiencies, and LPCI swing bus

transfer design deficiencies.

Additional -improved communicati_ons

with plant workers was encouraged during weekly tailgate meetings

which plant management frequently attended.- As such, policies

were well stated, diss~minated and understandable.

The lic~nsee's approach to the identification and resolution of

technical issue_s was excellent.

This was achieved by being

aggressive in creating an environment conducive to problem

identification, a willingness to expend resources to resolve

these i~sues and in most case~ a conservative approach in

regards to safety and compliance.

This approach permeated.the_

working levels as shown by the ~ignificant reduction* in the

number of LERs attributable to personnel *rrors. Of the LERs

i*ssued, .20 percent (8 of 41) were attributed to personnel error

during the previous period compared with 10 percent (5 of 50)

-during this period.

This trend showed improvement over four

"con s*ecut i ve periods. _The 1 i cen see' s cortect fve actions were, in

general~ encompassin~ and ~ffective: However, in one caie~

involving degradation of a fire barri~r, corrective actions were

  • fn retrospect too narrow in scope *to prevent a similar occurrence.

22

..

.

  • .

.The licensee identified past design problems as described in

section IV.F -0f this report and as indicated by the HPCI drain

pot piping thermal and seismic design discrepancies identified

by a licensee safety system functional inspection.

The licensee

was aggressive in finding, evaluating and conservatively rectifying

difficult equipment proble~s such as the LPCI outboard injection

-valve stem to plunger separationi the HPCI system feedwater

backleakage, and the recirculation pump innef seal cooler.

leakage events.

The licensee applied a low threshold for

issuance and resolution of deviation reports which aid~d in the

identification of and directed management attention toward

specific plant problems~

Th~ licensee's root cause analysis was aggressive and thorbugh

in arriving at the correct conclusions as exemplified by the

licensee's response to the January *16, 1990 loss of off site

power event.

In a few cases, the licensee's r6ot cause analy~is

was initially incorrect, such as th~ main generator reverse

power relay. failures, RPS motor generator (MG) set thermal

overload tiips, and main steam *line radiation monitor locku~s.

These events occurred more than once before the correct root

cause ~as -identified.

These cases were difficult to analyze and

  • it was only through the diligence of the 1 icensee that' correct

root causes were eventually determined.

Special investigation~

coordinated by the licensee's regulatory assurance organization

for issues such as the grease discovered on the torus to reactor

  • ,building* v~cuum breaker check valve seats were tho~ough and

comprehensive.

Management Is ability to. recognize and address adve.rse trends was

exemplified by the licensee's February 25, 1990 Unit 3 50

percent power plateau ~pecial review after the post-refueling

outage start up and. the licensee 1 s efforts to i ncreas.e the size

of the plant technical staff .. QA audits .were scheduled, based

on audit and assessment experience fo the prev.i ous year, to

effectively target problem are~s.

S~veral proposals to meet

requirements presented in initial lic~nsirig submittals were not

conservative with regards to safety.

These included station

blackout (SBO), wetwell venting, and post-accident hydrogen

control.

The initial response to the SBO rule did not significantly

improve the reljability of onsite or offsite power systems.

S~bsequent submittals and discussions r~sulted in the addition

of a diesel generator to improve the reliability of onsite

power.

This resolution wh~ch is under staff review, appears to

meet the SBO Rule.

The licensee's responsiveness to NRC initiatives was good.*

Respqnse to generic letters, bulletins and info.rmation notices

were timely.

On occasion, time extensions for responding to

regui'atory actions were requested and made.

These requests

resulted in a more comprehensive response.

A quality assurance

surveil 1 a rice conducted as a res1Jl t of NRC ,.conc_erns about an

.

.

23.

upward trend in outstanding control room work requests resulted

in specific actions to address and resolve the problem.

Another

exampl~ consisted of actions taken, including increased QA

~igilance and QC involvement, due to NRC concerns regarding

contractor control in the.previous assessment.

This resulted in

the on-schedule completion of the Unit 3 refueling outage with

few problems.

This was also aided by an increased emphasis on.

planning and staging of activities during the outage.

On a few

occasions, responsiveness to followup actions was not good.

Th~se included licensing resporise to the Salem ATWS Item 4.5.3,

the masonry walls, and the post-accident hydrogen generation

issues. The licensee's responsiveness was good with respect to*

allegations regarding unsealed fire openings inside conduit

  • penetrations in fire walls and pyrocrete covering polyurethane

in fire walls.

The licensee, in general, expedited thorough

responses to various inquiries originating with the NRC regional

and NRR staffs.

Licensee management at several levels aggressively

pursued continued good communicati~ns with the NRC resident

inspectors and NRR staff with the intent of sharing and resolving

concerns.

The licensee's Nuclear Tracking System ensured that

NRC findings and commitm~nts were a~propriately*proce~sed.*

Staffing as well

a~ the effectiveness of the training and

qualification ~rogram was excellent.

The licensee's site*QA and

QC organizations were staffed to ensure experience in a wide

range of disciplines .. The QA organization was c6mmitted to the

evaluatiori of ope~ational activities by having QA engineers.with

SRO licenses.

In addition, the QA supervisor was :experienced in.

radiatio~ prote~tion. The QA org~riization was especially

effective through.the performance of in-depth audits and

.surveillances ~f emergency preparedness, radiation protection,

and securiti activities.

On a routine and as needed basis, QA

also conducted reactive surveillances .. The seep~ and quality of

the audi*ts/surveillances were good in assessing technical

performance, compliance with NRC requirements, and training of

security personnel.

Licensee responses to QA security findings*

were timely and technically sound.

The auditors involved in

security were qualified and competent to perform their audit

responsibilities.

The licensee secur1ty organization also

established an internal audit function to supplement QA review

activities.

Both audit organization~ ~ere positi~e contributing

factors to the security organization's per.formance.

However,

the QA audits in the main~enance are~ were found not to be*

performance based during the first half of the period.

The

audits improved, in general, during the last half of the period

by incorporating a performance based m.ethodology.

The onsite

review committee was appropriately staffed with qualified

individuals ~esulting in generally comprehensive and thorough

reviews.

The Nuclear Safety Gr~up exceeded.Technical Specification

requirements by including an onsite as well as the required

offsite contingent.

The Nuclear Safety Group conducted quarterly

24

(

meetings with plant management to discuss recurring events,

corrective action evaluation and the results of various other

Nuclear Safety Group reviews.

This group was effective in

identifying adverse trends such as the timeliness of deviation

report processing.

Corporate assessments were conducted by

knowledgeable individuals. Management attention was directed

toward improvement in the QC group as exemplified by a staffing

increase and additional job s~ecific trainin~. The increased

competence of this group was shown by the ability of the QA

organization to release certain oversight functions back to the

QC group such as radwaste shipment reviews and receipt inspections.

Additionally, the QC organizational improvements resulted in

effective oversight of outage activities and an overall reduction

of *errors.

2.

Performance Rating

The licensee's performance is rated Category 2 improving in this

area.

The licensee's performance was rated Category 2 improving

in the previous assessment period.

3.

Recommendations

None.


~------

25

..

.. -*

v.

Supporting Data and Summaries

.A.

Licensee Activities

1.

Unit 2

Dresden Unit 2 began the SALP assessment period in a scheduled

maintenance outage, whi~h began on October 30, 1988.

Unit ~ was

returned to service from this outage on February 21, _ 1989, after*

which, the unit operated routinely at varied power levels

throughout the majority of the SALP assessment period including

reduced power loads and several short outages for maintenance,

surveillance and equipment repairs.

Unit 2 ended the SALP

operating routinely at full power.

Dresden Unit 2 experienced 12 ESF actuations (~ncluding two .

safety injection signals) and four automatic reactor scrams.

Three scrams occurred as the result 6f equipment failures, and

one was the result of a personnel error. * *

...

Significant outages and events ,which occurred during the SALP

assessment period are summarized below.

Significant Outages and Events

a.

  • During October 30, 1988 through February 21, 1989, Unit.2

was shutdown for i~s el~venth refueling outage.

.

.

  • b.

On March 4, 1989, Unit 2 scrammed due to the 1 oss of

reactor feedwater pump oil pressure control circuitry

duririg the 125 VDC battery ground checking. * Adjustments

and repairs were made, and the unit was returned to

service on Mar~h 6,

1989~

c.

d.

e:

During March 16~11, 1989, Unit 2 was shutdown *to perfori

. ov_erspeed trip setpofnt tests.

On July 12, 1989, Unit 2 scrammed due to a main steam line

(MSL) radiation moni~or spurious signal .. *The

11A

11 MSL

radiation monitor was replaced, and ~he unit was returned

to service on July 14, 1989.

On December 10, 1989, *un.it 2 shutdown for a planned maintenance

outage and restarted on December 20, '1989;

The major

activities inclu~ed facility testing of batteri~s.

On December 22, 1989, Unit 2 was separated from the grid

due to seal oil backing up into the generator casing.

It

was determined that a clogged seal oil fl oat trap caused

oil to overflow the hydrogen seal oil drain enlargement,

resulting in tiil backing up int6 the generator casing.

The unft was back on line December15; 1989.

26

..

g.

On January 5, 1990, Unit 2 experienced an automatic reactor scram as the result of procedural deficiencies

during a surveillance test such that inadequate controls

were provided to prevent a potential pressure transient .

.The unit was back on line January 10, 1990.

h.

. On January 16, 1990, Unit 2 experienced an automatic

_

reactor scram and a loss of offsite power as the result of

~ condensate ~ump failure and 'subsequent low vessel level.

The unit was returned to service on Ja*nuary 23, 1990.

2.

Unit 3

Dresden Unit 3 began the SALP assessment period operating at

approximately 97% power.

On December 3, 1989, refueling

activities began~ following a continuous operating run of 185

days.

Unit 3 was returned to service on February 10, 1990, and*

operated routinely through the remainder of the assessment *

period.

  • Dresden. Unit 3 experienced three ESF actuations (including one

safety injection signal) and four autcimatic reactor scrams~

  • All of the scrams occurred as either the result of equipment

.failures or spurious sign~ls during testing.

Significant outaQes and events that occurred during the SALP

assessment period are summ.arized below.

Significant Outages and Events

a.

On March 25, 198~, Unit 3 ~crammed and experienced a loss

of offsite power as the result of a 345-kV breaker

failure .. The unit was return~d to service on March 27,

1989.

  • b.

On March 30, 1989; Unit 3 experienced an automatic scram

due to a MSL radiation monitor spurious signal dur~ng RPS

EPA testing.

'Th~ unit was returned to service on April 1,

1989;*

c.

d.

e ..

On Aprii 15,* 1989, Unit 3 scrammed during turbi~e testing

a_s a result of a defective master-slave relay contact on

the No. 2 turbine stop valve.

The relay was replaced and.

the unit was returned to servfce on April 17, 1989.

During May 5-31, 1989, Unit 3 was shutdown for a scheduled

maintenanc~ outage to replace the degrading unit mai~

transformer.

During December 3, 1989, through Febn1ary 11, 1990, Unit 3

was shutdown for a scheduled refueling o~tage. The unit

completed a 185 continuous operatirig"run prior to the

outage.

27

....

f.

On February 11, 1990, Unit 3 was shutdown as a precaution

due to seal leakage on the B reactor recirculation pump.

The seal was verified to be operational and the unit was

returned to service on February_ 23, 1990.

g.

On March 10, 1990, Unit 3 scrammed as* a result of a MSIV

pilot air line failure.

The direct line was replaced and

other air lines were inspected .. The unit was returned to

service on March 11, 1990.

B.

Inspection Activities

Thirty~five inspection report5 are discussed in this SALP Report -

(February l, 1989 through April 30, 1990) and are listed in

Paragraph 1 of this section, Inspection Data.

Table 1 lists the

violations by fonctional areas and severity levels.

Significant

inspection activities are listed in Paragraph 2 of this section,

Special Inspection Summary.

1.

Inspection Data

Facility: Dresden Nuclear Power Station

Unit 2 Docket No.:

050-00237

Inspection Reports No.:

89005 through 89008, 89010 through

89026, and 90002 through 90012

Unit 3 Docket No.:

050-00249

Inspection Reports No.:

89005 thr6ugh B9026, and 90002 through

9001.1

-

TABLE 1

Number of Violations in Each Severity Level

Unit 2

Unit 3

Common

Functional Areas

III

IV

v III

IV

v

III

IV

v

-

a.

Plant Operations

1

1

b.

Radiological Controls

-

.1

c.

Maintenance/Surveillance -

1

2

1

d.

Emergency Preparedness

-

e.

Security

2

1

f.

Engineering/Technical

Support

1

g.

Safety Assessment/

Quality Verification

1

Unit 2

Unit 3

- .Common

  • . '.*.' . ~--*' .

TOTALS

III

IV

v-

III

IV

v

III

IV

v

2

2

.;..

6

2

28

....

2.

Special Inspection Summary

Significant inspections conducted during the Dresden SALP 9

assessment period ar~ listed below:

a.

b.

c.

d.

e.

On March 25~26, 1989, a team inspection was ccnducted as a

result of the Unit 3 scram and loss of off site power on

March 25, 1989 (Inspection Report Nos. 237/89005;

249/89005).

.

During April 17-21, 1989, a team inspecti~n**of the EQ

program was conducted (Inspection Report Nos. 237/89010;

249/89009).

.

.

During April 24-25, 1989, a special inspection of the

emergency ~reparedness program was conducted (Inspection

R~port Nos. 237/89014; 249/89013) ..

During July 31 - August 4, 1989, a team Regulatory

Effectiveness Review was c~nducted (Inspection Report

Nos. 237/89024; 249/89023).

During Octobe~ 31 - November 3; 1989, a team inspection of

the emergency preparedness exercise was conducted

(Inspection Report Nos. 237/89021; 249/89020) .. '*

. f.

DuriAg November 1-4, 1989, an-augmented inspectton team

inspec.tion_of the Units 2 and 3 HPCI waterhammer:events was

conducted (Inspection ~epor~*Nos. 237/89023; 249/89022).

g.

h.

i .

During January 9-24, 1990, an inspection of the emergency

preparedness program was .conducted (Inspection Report *

Nos. 237/90002; 249/90002).

During January 17-20, 1990, an augmented team inspection

of the Unit 2 January 16, 1990 loss of offsite power event

was conducted (Inspection Report No. 237/90004)

During April 10-13, 1990, a team. inspection Qf the

emergency preparedness exerciie was ~onducted (Inspec~ion

Report Nos. 237/90007; 249/90008). *

C.

Escalated Enforcement Actions

None.

D.

.Confirmatory Action Letters (CAL)

A CAL was issued on January 17, 1990, (CAL RIII-90-001) addressing

the root cause determination and corrective actions associated with

the Unit 2 reactor ~cram and loss of offsite p~wer ..

29

E.

Review of Licensee Event Reeorts (LERs}

Collectively, 50 LERs were issued during this SALP assessment

period, in accordance with NUREG-1022 guidelines.

Unit 2

LER Nos.:

89001 through 89032, and

90001 through 90003.

Unit 3

LER Nos.:

89001 through 89011, and

90001 through 90004.

Table 2 below, shows cause area counts by unit:

  • Table 2

Number of LERs by Cause

  • Cause Areas

Unit 2

Unit 3

Personnel Errors

2

3

Design Deficiencies

8

2

External

1

1

Procedure Inadequacies

10

4

Equipment/Component ..

13

5

Other/Unknown

0

1

TOTALS

34

16

Table 3 below shows a cause code comparison of SALP 8 and SALP 9:

Table 3

SALP 8

SALP .9

(12 Mo.)

.( 15 Mo.)

Cause Areas

No.

Percent

No.

Percent

Personnel Errors

8

19.5

5

10.0

Design Deficiencies

3

7.3

10

20.0

External

0

0.0

2

4.0

Procedure Inadequacies

11

26.8.

12

24.0

Equipment/Component

17

41. 5

20

40.0

Other/Unknown

2

4.9

1

2.0

--

TOTALS

41

100%

50

100%

Frequency LERs/Mo

3.4

3.3

NOTE:

  • The above LER information was derived from the:~evi~w of LERs

performed by the NRC staff, and may' not coincide with the licensee's

cause code assignments per NUREG-1022 guidelines.

30