ML17191A900

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Insp Repts 50-237/98-21 & 50-249/98-21 on 980714-0825. Violations Noted.Major Areas Inspected:Licensee Operations, Engineering,Maint & Plant Support & Included Reviews of Miscellaneous Insp Followup Items by Regional Inspectors
ML17191A900
Person / Time
Site: Dresden  Constellation icon.png
Issue date: 09/24/1998
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17191A898 List:
References
50-237-98-21, 50-249-98-21, NUDOCS 9810020067
Download: ML17191A900 (30)


See also: IR 05000237/1998021

Text

U.S. NUCLEAR REGULA TORY COMMISSION

REGION 111

Docket Nos:

License Nos:

Report No:

Licensee:

Facility:

Location:

Dates:

Inspectors:

Approved by:

9810020067 980924

PDR

ADOCK 05000237

a

PDR

. 50-237; 50-249

DPR-19; DPR-25

50-237/98021 (DRP); 50-249/98021 (DRP)

Commonwealth Edison Company

Dresden Nuclear Station, Units 2 and 3

6500 North Dresden Road

Morris, IL 60450

July 14 through August 25, 1998

K. Riemer, Senior Resident Inspector

D. Roth, Resident Inspector

B. Dickson, Resident Inspector

C. Brown, Reactor Engineer, Riii

P. Lougheed, Reactor Engineer, Riii

R. Langstaff, Reactor Engineer, Riii

R. Lerch, Project Engineer, Branch 1 Riii

G. O'Dwyer, Reactor Engineer, Riii

M. Ring, Chief

Reactor Projects Branch 1

EXECUTIVE SUMMARY

Dresden Nuclear Station Units 2 and 3

NRC Inspection Report 50-237/98021(DRP); 50-249/98021(DRP)

This inspection included routine resident inspection from July 14, 1998, through

August 25, 1998, augmented by regional inspectors.

This inspection also included aspects of licensee operations, engineering, maintenance, and

plant support, and included reviews of miscellaneous inspection followup items by regional

inspectors.

Operations

The licensee planned power change evolutions well and executed troubleshooting

activities in accordance with the plans. Operators performed the evolutions in a

deliberate and controlled manner (Section 01.2) ...

The licensee declared the Unit 2 HPCI system inoperable during this inspection period

due to the failure of the trip solenoid valve. The symptoms of this failure were similar to

an earlier failure (Section 02.1 ).

Routine performance was generally acceptable (Section 04.1).

During this inspection period, the operators violated Technical Specifications during

movement of spent fuel. The failure to recognize entry conditions and action

  • statements of the Technical Specifications continued a negative trend (Section 04.2).

Maintenance

The inspectors identified no concerns with jobs directly observed (Section M1 .1).

Material condition issues continued-to adversely affect plant operations. Some of these

issues represented rework for the maintenance organization (Section M2.1).

The inspectors noted discrepancies between .administrative and procedural

requirements for independent verification. The licensee's Nuclear Oversight group also

identified this issue and was pursuing it through the corrective action process

(Section M3.1).

Failure to execute procedures correctly resulted in the generation of an unexpected

half-scram and disabled part of a reactor core protective feature. Independent

verification, as implemented in this case, failed to prevent the error (Section M4.1),

Poor work practices on the refuel floor presented an unnecessary challenge to control

room operators (Section M4.2).

2

Engineering

The repetitiveness of several items indicated that corrective actions had not always

been effective at eliminating the concerns (Section E1 .1).

Plant Support

Breakdowns in licensee processes and practices resulted in the release of

contaminated soil from the site (Section R4.1).

3

Report Details

Summary of Plant Status

Unit 2 began this inspection period at full power. On August 6, 1998, the generator was taken

off line to address a generator ground problem. The problem was addressed, the generator

placed back on line and near-full power restored by August 10, 1998. Return to full power was

delayed until August 13, 1998, due to a moisture separator high level alarm. After the alarm

was addressed, the unit returned to and remained at full power for the remainder of the

inspection period.

Unit 3 remained at full power throughout the inspection period, except for small decreases to

support maintenance and surveillance testing.

Full power c;m both units was limited by the maximum steam flow allowed by the analysis for an

anticipated transient without scram (A TWS) event. The licensee had not completed actions to

remove the limit during this period.

I. Operations

01

Conduct of Operations

01.1

General Comments (71707)

Using Inspection Procedure 71707, the inspectors conducted frequent reviews of.

ongoing plant operations. Specific events and noteworthy observations are detailed in

the sections below.

During the inspection period, some events occurred for which the licensee was required

by 10 CFR 50.72 to notify the NRC. The events and notification dates are listed below:

07/30/98

08102198

(Unit 2) High pressure coolant injection (HPCI) system

declared inoperable due to the inability to trip the turbine

using the remote turbine trip push-button during

operability surveillance testing.

(Unit 2) Partial Group I isolation caused by blown

, fuse while changing main control room main steam

isolation valve*(MSIV) light indication. The

licensee subsequently retracted this notification.

4

01.2 Down Power Evolutions in Support of Troubleshooting Activities (Unit 2)

a.

Inspection Scope (71707)

The licensee performed two downpower evolutions to support troubleshooting activities

associated with Unit 2. The inspectors reviewed licensee preparations for the down

power evolutions and observed operators' performance of the unit power

manipulations.

b.

Observations and Findings

Intermittent Generator Field Grounds

Over several weeks, Unit 2 experienced many, intermittent main generator/exciter

ground alarms in the main control room. The alarms were of short duration and cleared

themselves with no operator action. The frequency of the alarm occurrence increased

. to the extent that the alarms were being received every several minutes.

On August 6, 1998, the licensee decreased reactor power to approximately 25 percent*

to 35 percent to facilitate the installation of temporary monitoring equipment to aid in

troubleshooting of the ground location. The licensee, with General Electric assistance,

evaluated the data results to determine an appropriate permanent repair. The licensee

took the main generator off-line August 8, 1998, to perform minor cleaning and

refurbishment activities on the main generator and exciter. During the cleaning and

inspection activities, electrical maintenance personnel discovered the source of the

ground. The insulation on a cable inside the generator exciter housing had chafed

against a support and worn away which allowed the conductor to contact ground. The

licensee repaired the cable and returned the unit to service on August 9, 1998.

Operators properly performed the power change evolutions in accordance with station

procedures. The control room atmosphere was professional and management

exercised good overall control throughout the maintenance activities. The outage was

also well planned and executed from a maintenance perspective.

Moisture Separator Drain Tank Hi Level Alarm

The Unit 2 operators received a moisture separator high level alarm during power

ascension activities following the downpower for troubleshooting and repair of the main

generator ground. An automatic turbine trip and reactor trip occurs approximately

4 inches above the alarm setpoint. Operators lowered reactor power to clear the alarm.

The licensee developed a troubleshooting plan which entailed temporarily disabling the

high level trip to troubleshoot the causes of the alarm. The plant operations review

committee (PORC) aggressively reviewed the proposed plans and rejected the initial

proposal to troubleshoot the concern. Plant staff revised the package to address the

PORC concerns and presented the package to the PORC again. F:ollowing PORC

approval of the revised plans, the licensee attempted to re-create the alarm condition

5

c.

and eliminate the alarm. The licensee was unable to re-create the high level alarm and

operators returned the unit to full power. The alarm did not actuate in again during the

inspection period.

Conclusions

The licensee planned the power change evolutions well and executed the

troubleshooting activities in accordance with.established plans. Operators performed

the downpower evolutions in a deliberate and controlled manner.

02

Operational Status of Facilities and Equipment

02.1

High Pressure Coolant Injection (HPCI) System

a.

Inspection Scope (71707)

b.

The inspectors reviewed the status of the Unit 2 HPCI system.

Observations and Findings

On July 30, 1998, the licensee performed the quarterly operability surveillance for the

Unit 2 HPCI system. During the test, the HPCI system's turbine stop valve failed to

close when an operator depressed the remote turbine trip push button. The licensee

declared the Unit 2 HPCI system inoperable.

During troubleshooting, the licensee identified that.soldering for leads from the HPCI

turbine trip solenoid to the 125 VDC circuit had failed. The termination points for these

leads were inside the body of the trip solenoid. After the licensee resoldered the leads,

the licensee tested the HPCI system turbine stop valve successfully.

The licensee had previously declared the Unit 2 HPCI system inoperable on April 17,

, 1998, due to the inability to trip the HPCI turbine using the remote push-button. Then,

a licensee investigation concluded that the contacts used to connect the 125 VDC

circuit to the HPCI turbine trip solenoid valve were faulty due to corrosion. Thb licensee

suspected that the corrosion caused a momentary loss of continuity across the circuit.

As corrective action, the contacts were cleaned.

This July 1998 event was similar to the April 1998 HPCI failure in that the material

condition of the HPCI trip system caused the licensee to declare the HPCI system

inoperable.

c.

Conclusions

The lrcensee declared the Unit 2 HPCI system inoperable during this inspection period

due to the failure of the. trip solenoid valve. This failure was similar to an earlier failure

that caused the licensee to declare the HPCI system inoperable .

6

04

Operator Knowledge and Performance

04.1

Routine Operations (Units 2. 3)

'

a.

Inspection Scope (71707)

The inspectors observed control room and field activities and compared operator

performances with the licensee's standards and procedures.

b.

Observations and Findings

Usually, the operators performed their assignments satisfactorily. Turnovers were

informative. The operators were aware of plant conditions and equipment status and

could readily answer questions about plant performance.

However, the inspectors noted instances where operator performance was lacking,

including an example where a nuclear station operator (NSO) performed an inadequate

independent verification of a relay jumper connection. This example is discussed in

Section M4.1 of this report; the remaining examples follow~

Inadvertent Manual Start of 3C Low Pressure Coolant Injection (LPCI} Pump

On August 8, 1998, maintenance personnel were inspecting and troubleshooting the

3C containment cooling service water (CCSW) pump. As part of the troubleshooting

effort, maintenance personnel requested that operations staff start the pump so the

packing could be adjusted as needed.

After a review of the appropriate procedures for starting the 3C CCSW pump, an NSO *

proceeded with actions to start the pump. At this point, the NSO .took control of the

wrong control switch and inadvertently started the 3C LPCI pump. The NSO

immediately recognized the incorrect pump start and secured the LPCI pump.

A licensee investigation concluded that the inadvertent CCSW pump start was due in

part to two reasons: 1) Unawareness. An insufficient degree of attention was applied

to the task, and 2) Mindset. A frequently performed task (starting a pump) was not

completely reviewed for expected actions. The licensee also concluded that the NSO

did not give others an opportunity to peer check actions to be taken and review the

control switch to be manipulated.

In Inspection Report (IR) 98019, Section 04.1, the inspectors noted a lack of consistent

self-checking or peer review during control panel manipulations. Self-check and

  • solicitation of peers are suggested standards in Dresden Administrative Procedure

(DAP) 05-45, "Operations Standards."

This event emphasized the importance of self-checking and the solicitation of peer

review when performing manipulations on the control panel.

7

c.

Unrecognized Emergency Lighting Dresden Administrative Technical Requirement

(DATR) Limiting Condition of Operation (LCO) .

On July 28, 1998, the licensee identified that operators failed to enter the appropriate

DA TR LCO for safe shutdown lighting when maintenance personnel disabled lighting

circuits 354 and 355 for battery discharge testing. The DA TR LCO limitations were not

exceeded, however, this represented another example where operating personnel

failed to recognize entry into an LCO. In addition, operations staff failed to recognize

that the ongoing maintenance work was unauthorized when originally contacted by

maintenance personnel.

Conclusions

Routine performance was generally acceptable. However, instances occurred where

operator performance was lacking, including a wrong component manipulation and an

example of operator lack of awareness of a DA TR LCO condition.

04.2

Unrecognized Entries into LCO

a.

Scope

On August 6, 1998, operators missed required entries into Technical Specification (TS}

LCOs for suppression chamber and drywell spray (TS 3.7.L} and suppression pool

cooling (3.7.M}. The inspectors reviewed the circumstances associated with the

operators' lack of recognition of the required TS LCO entry conditions.

b.

Observations and Findings

Failure to Recognize Entry into LCO Conditions

On August 6, 1998, operators entered a 4-hour LCO per TS 3.7.D (Primary

Containment Isolation Valves} to support testing of the M03-15Q1..;5D, 3D low pressure *

coolant injection (LPCI} suction valve. Maintenance department personnel were unable

to complete the testing activities successfully and return the valve tQ an operable status

within the 4-hour period. Operators shut the 3-1501-338, (LPCI Division II, manual

suction isolation valve} to comply with the primary containment isolation requirements

of TS 3.7.D. Upon shutting the 338 valve, operators appropriately entered TS 3.5 for

an inoperable LPCI subsystem. However, operators failed to recognize two additional

TS LCO entry conditions. With an inoperable LPCI subsystem, operators should also

have entered TS 3.7.L, for suppression chamber and drywell .spray and TS 3.7.M for

suppression fuel cooling. All of the required TS were 7-day LCOs. The subsequent

two operating shifts also missed the required TS LCO entry conditions.

The following morning, a Station Nuclear Oversight individual reviewed problem

identification forms from the previous day and questioned whether the operators had

identified all appropriate TS LCO entry conditions. Following conversations among

station personnel, operations correctly entered the additional TS LCOs and dated the

8

entries to the original time of equipment inoperability. The station documented the

occurrence via problem identification form 01998-04696, initiated a Prompt

Investigation into the matter, and incorporated the event into a prior trend investigation

report (Investigation 237-230-98-00800, Adverse Trend in LCO Management).

The licensee did not exceed the times specified in the LCOs for suppression chamber

and drywall spray or suppression pool cooling. Therefore, the licensee did not violate

the applicable TS. However, the failure to recognize the required entry conditions

continued an adverse trend, first documented in IR 50-237/249-98019. Inspection

Report 50-237/249-98019 documented the issue in a noncited violation for two

examples of failing to recognize TS LCO entry conditions. Licensee actions taken in

response to the prior occurrences were not effective in preventing another occurrence

of operators failing to recognize TS LCO entry conditions.

,

The failure to recognize and log entries into the two LCOs violated the administrative .

requirements of the TS. Dresqen TS 6.8.A, stated, "Written procedures shall be

established, implemented, and maintained covering the activities referenced below:

1. The applicable procedures recommended in Appendix A, of Regulatory Guide 1.33,

Revision 2, February 1978." Appendix A of Regulatory Guide 1. 33 recommended

administrative procedures for log entries. Dresden Administrative Procedure

(OAP) 07-25, "Operating Charts, Logs and Records," Revision 27, Step E.2., stated,

"The following outlines the requirements for log keeping: .... c.(4) If any activity results

in an LCO condition, the Tech Spec and the applicable actions shall be clearly

identified."

  • Contrary to the apove, operators failed to identify the entry into the LCO conditions for

suppression chamber and drywell spray, and failed to identify the entry into the LCO for

suppression pool cooling. However, the NRC refrained from issuing a violatior:i in this

case because the issue of recognition of TS LCO entry conditions was identified as a

noncited violation in Inspection Report 98019 and corrective actions may not have had

sufficient time to be fully effective. The inspectors noted that during this inspection

. period, there were three issues related to recognition of entry into TS (see

Section 04. 1 ). These examples continued an adverse trend first documented in the

prior inspection report.

Failure to Comply With Control Room Emergency Ventilation System TSs

On August 20, 1998, operators violated the requirements ofTS 3.8.D (control room

emergency ventilation system) by granting permission to perform a fuel bundle move .

while the refrigeration control unit (RCU) was inoperable. The inspectors reviewed the

circumstances associated with the event.

On August 20, 1998, operators established an out-of-service to support repair of the

control room RCU service water inlet valve. The repair was an emergent item due to

increased valve leakage; as a result, the licensee changed the work schedule. The

hanging of the out-of-service tags rendered the RCU inoperable and operators

9

c.

appropriately entered TS 3.8.D for an inoperable RCU. The work schedule already

contained an item to move a damaged fuel bundle from the spent fuel pool to the fuel

prep machine to support inspections on the bundle.

While operators correctly recognized that an inoperable RCU required entry into

TS 3.8.D, they did not realize all of the requirements of the TS, and, so, failed to

comply with the TS. While in OPERATIONAL MODE 1, 2, or 3, an inoperable RCU

resulted in a 30-day LCO. This was the part of the TS that the operators recognized.

However, the TS is also applicable to mode "*" which applies, "When handling

irradiated fuel in the secondary containment, during CORE ALTERATION(s), and

operations with a potential for draining the reactor vessel." The TS states that while in

OPERATIONAL MODE"*" with an inoperable RCU, immediately suspend Core

Alteration(s), handling of irradiated fuel in the secondary containment and operations

with. a potential to drain the reactor vessel. When refuel floor personnel moved the

damaged fuel bundle, after receiving control room permission, the licensee violated the

requirements of TS 3.8.D.

The station missed multiple opportunities to prevent the error. The operators who

reviewed the work package and associated out-of-service on the shift before

commencing work failed to catch the conflict between the scheduled fuel move and the

emergent valve repairs. The operators who established the out-of-service and granted

permission to perform the fuel move, repeated that failure. A heightened level of

awareness briefing conducted before the fuel bundle move did not contain complete

discussion concerning TS requirements. The fuel handling supervisor, licensed as a

senior reactor operator limited to fuel handling (SRO-L), also failed to understand the

TS requirements. The violation of TS requirements went undiscovered for 1 day. On

August 21, 1998, fuel handling personnel requested permission to resume movement

of the fuel bundle. A different unit supervisor was on the shift that day and recognized

the conflict between fuel movements and an inoperable RCU. Based on discussions

with the fuel handling supervisor, the unit supervisor. realized that the licensee violated

TS 3.8.D the previous day. The licensee documented the TS violation via problem

identification form 01998-04845 and initiated a prompt investigation to learn the cause

and proper corrective actions.

Dresden TS 3.8.D, stated that when in OPERATIONAL MODE "*"with an inoperable

RCU, "immediately suspend CORE AL TERATION(s), handling of irradiated fuel in the

secondary containment, and operations with a potential for draining the reactor vessel."

Contrary to the above, on August 20, 1998, the licensee moved an irradiated fuel

bundle in the secondary containment while an RCU was inoperable. This action was a

violation of TS 3.8.D (VIO 50-249-98021-01(DRP)).

Conclusions

Operator failures to recognize applicable TS LCO entry conditions and action statement

requirements continued a negative trend first documented in the prior NRC inspection

report (IR 50-237/249-98019(DRP)). The licensee's immediate corrective actions were

ineffective in stopping the trend. Of concern was the fact that the operations

department did not identify all of the TS discrepancies. The prior inspection report

10

08

08.1

08.2

documented examples where the operators demonstrated a lack of recognition of TS

LCO entry conditions; however, the licensee did not violate the TS requirements .

themselves. During this inspection period, one instance of operator non-recognition of

TS entry conditions resulted in a violation of the actual TS requirements.

Miscellaneous Operations Issues

{Closed) Inspection Follow-up Item 50-237/249-95009-02: Out of Service and

Equipment Configuration Control Problems. Beyond immediate corrective actions such

as comprehensive plant walkdowns and trend reviews, the licensee implemented more

rigorous controls on plant work and manipulation of equipment. While some

configuration control problems still exist, they are better tracked and reviewed as part of

routine resident core inspections. This item is closed.

{Closed) Licensee Event Report CLER) 237/90002-02: Reactor Scram Following

Condensate/Condensate Booster Pump Failure Due to Internal Failure. Revision 2 of

the LER was issued October 6, 1995, to clarify methods used to perform 4KV motor

insulation testing. The NRC has reviewed and closed the previous revisions of this

LER. The inspector had no concerns or questions regarding the additional information

provided This item is closed.

08.3

{Closed) LER 237/95006-00: TIP System Isolation Does not Have "Seal in" Logic on

Group II Isolation. The licensee reviewed the licensing basis and concluded that the

requirement for seal-in protection was not clear; however, the licensee modified the

system to add the seal-in logic function so that the TIP system isolation valves will not

automatically reopen when a Group II isolation signal is reset. This item is closed.

08.4

{Closed) LER 249/95-001-01: Scram From Main Turbine Stop Valve Closure Due to

Moisture Separator Level High High

Revision 1 to this LER modified the corrective action for the engineering department to

include training on the Stop, Think, Act and Review process. This item is closed.

08.5

{Closed) LER 249/95008-01: Unit 3 Scram From Main Turbine Stop Valve Closure Due

. to Turbine Trip on High Vibration Caused by Out of Specification Turbine Blade

Material. The licensee performed a thorough review of the reactor scram and plant

performance. The licensee adequately addressed the problems as evidenced by no

subsequent problems related to the scram. This item is closed.

08.6

{Closed) LER 249/95010-00: Inadequate LCO Entry Due to Inadequate Control of

Decay Heat During Cooldown. The operations staff failed to control reactor pressure

when too many steam loads were secured during a cooldown. Pressure increased to

greater than 150 psi and operations personnel had already taken the isolation

. condenser out-of-service. This resulted in the plant being in an unplanned limiting

condition for operation. The inspectors concluded that the licensee's corrective actions

were effective. Operations personnel performance with respect to control of plant

transients has improved. Inspection of plant operations will continue as part of the core

inspection program. This item is closed .

11

08.7

(Closed) LER 237/95013-00: Inadequate Sampling of Service Water Effluent Due to

Use of a Superseded Procedure and Recent System Configuration Change. The

inspectors concluded that the licensee's corrective actions of revising procedure

controls and retraining equipment attendants were adequate. The samples taken *

before, during, and after the problem were acceptable. This issue was of minor

significance, which would not be subject to formal enforcement action in accordance

with NUREG 1600, Rev. 1. This item is closed.

08.8

(Closed) LER 237195015-00 and 01: Leakage Limit Exceeded Due to Excessive

Leakage Past Main Steam Isolation Valves. The licensee refurbished two main steam

isolation valves. Refurbishment of the remaining valves is dependent upon leak rate

test results. Test results have improved due to better maintenance of the seating

surfaces. The licensee reported the failure of two additional valves in LER 237 /98004

and a supplement to the LER will provide the causes and corrective actions when the

licensee determines them. This item is closed.

08.9

(Closed) LER 237/95017-00: Containment Cooling Service Water Vault Penetration

Seals Failed Leak Test Due to Being Out of Adjustment. The licensee attributed this

problem to new seals. Tightening the seal connectors corrected the leakage.

Corrective action was to increase the testing frequency when the licensee installs new

seals. The leakage identified was very small; therefore, this event was of minor

significance, which would not be subject to formal enforcement action in accordance

with NUREG 1600, Rev 1. This item is closed.

08.10 (Closed) LERs 237/97013-00. 237/97014-00. 249/97014-00. 249/98001-00,

249/98002-00, and 237/98009-00: High Pressure Coolant Injection System Inoperable

Due to Gland Seal Leakoff (GSLO) Condenser Level Control Malfunction.

On several occasions the licensee declared the Unit 3 HPCI system inoperable due to

the failure of the GSLO condenser level co*ntrol switch to control level in the GSLO

condenser hotwell automatically. To remedy this, the licensee has completed several

. corrective actions to alleviate this reoccurring problem. One example included a design

change of the type of level control switch used in the GSLO condenser. The original

,

design used a float-type mechanism which consisted of mechanical linkages. The

newer design consisted of electromagnetic contacts which should be more reliable.

Since February 1998, with only one exception (May 4, 1998, Reference LER 98009),

the licensee has successfully completed several performances of Dresden Operating

Surveillance (DOS) 2300-09, "HPCI Gland Seal Leak Off Drain Pump and Condenser

Hotwell Level Control Function Test." Initially, these tests were performed weekly.

Presently, the licensee is performing this test monthly.

The inspectors will continue to follow this issue through routine inspection efforts ..

These items are closed .

12

II. Maintenance

M1

Conduct of Maintenance

M1 .1

General Comments

The inspectors monitored routine maintenance activities through direct observation,

attendance at maintenance and operations meetings, and by reviewing the results of

maintenance.

The inspectors identified no concerns with jobs directly observed. The mechanics and

technicians followed their procedures and work instructions, and correctly documented

the results. Inspectors routine review of issues identified in problem identification forms

(PIFs} revealed some issues in rework and work planning and scheduling, however,

these issues were not safety significant.

Nonetheless, as described in Section M2.1 of this report, the material condition of the

plant significantly challenged smooth full-power operations.

M2

Maintenance and Material Condition of Facilities and Equipment

M2.1

Maintenance and Availability of Equipment

a.

Inspection Scope (62707)

The inspectors reviewed the licensee's response to some self-revealing events in which

safety-related equipment w~s made unavailable after maintenance, or could not be

restored to operable following maintenance.

b.

Observations and Findings

The inspectors noted that several material condition issues and self-revealing

equipment failures during the inspection period required plant personnel to take prompt

action. The inspectors reviewed the failures to determine the effect on plant safety.

Control Rod Drive (CRD) H-12

On August 12, 1998, 20 minutes after insertion from Position 12 to Position 10 for flow

control line adjustments on Unit 2, CRD H-12 drifted back out of the reactor core to

  • Position 12. The event was identified after the operators received a ROD DRIFT

annunciation in the control room. The licensee performed a prompt investigation to

figure out the cause of the control rod drift. The investigation concluded after a review

of operator actions and procedures that human performance or procedural issues did

not cause this event. The CRD system engineer contacted the CRD expert from

General Electric Company for assistance during this investigation; there were two

hypothetical possibilities for this CRD anomaly included in the engineer's investigation

report.

13

Hypothesis #1.

Hypothesis #2 ..

"The control rod was not fully driven past the latching notch and

the coll et. fingers were just barely hung up on the edge of the

notch. Then after 19 minutes of reactor vibration, the rod drifted

to the next positive notch, Position 12."

"The control rod was not fully driven past the latching notch and

the collet fingers were just barely engaged in a small indentation

created from corrosion of the nitrated surface of the index tube.

This was concluded as somewhat unlikely."

To ensure this event would not recur, the system engineer recommended that when

inserting control rods, the operators should insert the control past the notch until the

control rod position indication system showed "blank" or the "odd" position above the

target position.

After several movements without the anomaly occurring again, the licensee declared

CRD H-12 operable and commenced CRD movements.

  • Circulation Water Pump

On July 20, .1998, the licensee identified a leak on the suction piping of the 2A

circulating water pump. Initially the leak was from a 3-inch circumferential crack in the

pipe near the base of the pump. Increased monitoring by the licensee revealed that the

crack grew from* 3 to 7 inches during 3 days.* The licensee repaired the leak.

Shutdown Cooling Pump

On July 16, 1998, during a monthly rotation check, the pump shaft for the 28 shutdown

cooling pump dropped approximately 2 inches while the pump was operating. After the

operators stopped the pump, the pump shaft returned to normal. The licensee

replaced the bearing and was continuing troubleshooting efforts on the shutdown

cooling pump at the end of the inspection period.

213 Emergency Diesel Generator (EOG).

On August 21, 1998, during prechecks for the 2/3 EDG monthly operability surveillance,

the operators discovered one of the twenty cylinder test valves out of position.

Licensee investigations concluded the apparent cause of the mispositioned valve was

vibration. The EDG vendor representative confirmed that there have been instanc.es

where the valve had vibrated open.

Reactor Water Cleanup (RWCU) System

RWCU Auxiliary Pump

At the end of the inspection period, the licensee discovered the suction valve

(3-1201-3) for the Unit 3 RWCU auxiliary pump leaking by, causing pressurization in

14

the pump. The pressurization could cause the pump seal to degrade. The licensee

physically isolated the auxiliary pump from the system. The RWCU auxiliary pump was

normally used to force flow through the RWCU system during periods of low reactor

pressure.

In Inspection Report 98014, Section M2.2, the inspectors documented an instance

where failure of the RWCU auxiliary pump adversely impacted the ability of Unit 3

operators to maintain reactor water level during shutdown and cooldown following the

reactor scram on May 17, 1998. The auxiliary pump has not been available for use

since that event despite the licensee's completion of repair efforts. The unavailability

was caused by operators inability to run and vent the system because the RWCU

system had been maintained at high pressure.

38 RWCU Pump

The licensee discovered excessive leakage on the 38 RWCU pump and discharge

valve. After multiple attempts to repair the pump and discharge valve the leakage

continued through this inspection period. This continued leakage represented rework

for the maintenance organization.

Unit 3 Isolation Condenser Condensate Return Outboard Isolation Valve

On August 10, 1998, after performing quarterly valve timing on the isolation condenser

valves, the main control room Isolation Condenser Temp Hi alarm annunciated. The

receipt of the high temperature alarm was a repeat event. Leakage past the

3-1301-3 valve (Unit 3 isolation condenser condensate return outboard isolation valve)

was suspected as the most likely reason for the high temperature in the isolation .

. condenser. In response to earlier NRC questioning about the system, because of a

prior alarm, the licensee provided documentation that the leak rate testing results and

motor operator testing results were satisfactory. The failure of the 3-1301-3 valve to

seat fully was an intermittent problem that only occurred when the valve was operated

from the control switch on the main control room.903-3 panel. This would suggest that

the high temperature conditions and subsequent main control room alarms were not a

result of poor valve material condition. The inspectors will evaluate licensee resolution

of the matter via routine resident inspections of plant material condition.

Dresden Nuclear Oversight individuals identified an additional concern associated with

the high temperature alarm issue. Operators were inconsistent in the manner in which

they responded to the high temperature alarm. In one instance, operators cycled the

isolation condenser valves following the annunciator procedure in an attempt to clear

the alarm, but did not declare the isolation condenser inoperable while doing so, nor did

they enter the LCO for the isolation condenser. Other times, operators cycled the

isolation condenser valves and declared the isolation condenser inoperable and .

entered the appropriate TS LCO. The licensee documented the valve concerns and

operator concerns via Problem Identification Forms (PIF) 019998-04844, 01998-04841

and 01998-04872. The TS LCO question is enveloped by .the NRC concerns with

respect to operator recognition of TS LCO entry conditions and will be tracked by NRC

15

follow up of licensee actions in response to the violations referenced in this report

(Section 04.2).

c.

Conclusions

Material condition issues continued to adversely affect plant operations. Some of these

issues represented rework for the maintenance organization.

M3

Maintenance Procedures and Documentation

M3.1

Independent Verification

a.

Inspection Scope

The inspectors interviewed licensee personnel and reviewed maintenance procedures

against requirements contained in administrative procedures. The inspectors reviewed

Dresden Instrument Surveillance (DIS) 500-06, "Condenser Low Vacuum Pressure

Switch Channel Calibration and Channel Function Checks" against OAP 07-27

"Independent Verification."

b.

Observations and Findings

The inspectors noted discrepancies between requirements shown in OAP 07-27

"Independent Verification" and various maintenance procedures.

The policy statements in OAP 07-27 stated that when an action or-manipulation (e.g.,

installing a jumper, lifting an electrical lead, operating a switch or breaker) could result

in an immediate threat to safe and reliable plant operation, a "second check" should be

performed instead of an independent verification. In OAP 07-27, the licensee defined

an independent verification as the act of checking a component position independently

of activities related to establishing the component's position (i.e., "Apart in time"). A

second check was defined as positively identifying the correct unit, train, or component,

and reviewing the intended action and expected response before performing the task to

prevent an unintended plant response (i.e., "Apart in Action").

On August 18, 1998, the inspectors questioned the licensee concerning this issue. The

licensee was aware of the discrepancies between OAP 07-27 and actual verification

techniques required in several surveillance tests and used in field work. The licensee

Nuclear Oversight group identified this issue thoroughly in a PIF 1998-04768, on

August 13, 1998. The licensee assigned both the operations and maintenance

organizations to revise the administrative procedures to provide clarity on the types of

verification techniques to be used when performing work activities. The licensee also

assigned the two groups to perform an apparent cause evaluation.

c.

Conclusion

. The inspectors noted discrepancies between requirements shown in OAP 07-27

"Independent Verification" and various maintenance procedures. The licensee's

16

M4

Nuclear Oversight group was aware of these discrepancies and the licensee has taken

steps to address them .

Maintenance Staff Knowledge and Performance

M4.1

Inadvertent Half-scram Caused by Instrument Maintenance Personnel Performance

a.

Inspection Scope (62707)

On July 31, 1998, an unexpected half scram was generated in the Unit 2 control room

during the performance of an instrument surveillance. The inspectors reviewed the

  • activities that caused this event.

b.

Observations and Findings

. On July 31, 1998, Instrument Maintenance (IM) Department personnel performed

Dresden Instrument Surveillance (DIS) 500-06, "Condenser Low Vacuum Pressure

Switch Channel Calibration and Channel Function Checks." This surveillance included

steps to jumper the "Low Condenser Vacuum" scram inputs in the reactor protection

system (RPS) logic string. This was done to prevent the receipt of half-scrams during

this surveillance. The licensee adopted this concept as part of its scram reduction

effort.

The licensee planned to remove the condenser vacuum pressure switches (503A, B, C,

and D) from service by attaching a RPS test box to each relay terminal. Each

condenser vacuum switch was to be bypassed,* calibrated and functionally tested

individually. The relays used in this application are HFA-type relays and are on

Panel 902-15 in the main control room. The licensee installed banana jacks on specific

relay terminal posts for ease of landing the leads to the relay.

The Instrument Maintenance Departmen't (IMO) personnel performing the test had

signed off steps indicating pressure switch 2-503A had been removed from service and

. *"

were testing the channel circuitry, when an unexpected half scram signal was received

in the control room. Step 8.a.3 of DIS 500-06 required installation of the RPS test box

leads to terminals 2 and 4 of relay 590-101A. The IMO personnel mistakenly installed

the leads to relay 590-107C (Average Power Range Monitor (APRM) channel #3). The

error occurred even though the DIS included a barrier of independent verification during .

installation of the jumper. A Unit 2 nuclear station operator (NSO) had attempted to

perform the independent verification.

The relays involved in this event were adjacent, but there was reasonable separation

between the two relays. Also, the relays were labeled appropriately.

The licensee performed a prompt investigation into the cause of the vent, and

concluded the cause was "the failure of the IMO Tech and the NSO to perform self-

checking" following a momentary interruption in work. The investigation also stated, "It

was apparent that proper verification techniques were being utilized.during the

. performance of the relay identification."

17

The inspectors independently investigated the event and found that differing causes

existed that were not identified by the licensee. Specifically, the inspectors concluded

that, contrary to the prompt investigations's findings, proper verification techniques

were NOT used. The NSO did not perform an independent verification, but instead

performed the verification concurrently with the instrument mechanic. Dresden

Administrative Procedure (OAP) 07-27, "Independent Verification," defined an

independent verification as the act of checking a component position independently of

activities related to establishing the components's position (i.e., "Apart in time").

Dresden TS 6.8.A required that written procedures be implemented .covering the

applicable procedures recommended in Appendix A of Regulatory Guide (RG) 1.33,

Revision 2, February 1978. Appendix A of RG 1.33 recommended both procedures for

surveillance and calibration tests and for administrative procedures.

Step 6.a.3 of DIS 500-'06 required that leads from the RPS test box be landed on Relay

Post 2 and 4 for relay 590-101A. Step 6.a.6 of DIS 500-06 required that IM personnel

actions be independently verified.

Contrary to the above, on July 31, 1998, the licensee incorrectly installed the jumper on

Relay 590-107C and the independent verifier failed to perform an adequate

independent verification in accordance to OAP 07-27.

As a consequence, APRM #3 protective features were bypassed without the operators

being aware of it, and eventually an unexpected half-scram occurred. Failure to follow

procedures for installation of a jumper on relay 590~101A was considered a violation of

TS 6.8.A (VIO 50-237/98021-02(DRP)).

'

.

This is being treated as a violation consistent with NRC Enforcement Policy

(NUREG 1600) Section Vll.B.1 which states, in part, that licensee identification credit is

not warranted when a licensee identifies a violation as a result of an event where the

root cause of the event is obvious. The inspectors also concluded the licensee's

investigation was superficial and the corrective action defaulted to the easy fix of

coaching the involved individuals.* The licensee's prompt i~vestigation failed to identify

or correct the discrepancies between independent verification requirements described

in the administrative procedure and the actual verification techniques used while

performing the surveillance.

Subsequent to the event, but prior to the inspectors identification of the violation, the

licensee Nuclear Oversight (NO) organization performed an inspection of independent

verification. The NO organization found that independent verifications were not always

being performed correctly. As a *result, the licensee instituted the appropriate corrective

actions (reference Section M3.1). Therefore, no response is required for this violation.

In addition to the causes of the event, the inspectors also assessed the impact of the

error on the plant. The incorrect installation of the RPS test box on 590-107C removed

Unit 2's APRM #3 from service. Nothing on the control panels alerted the operators of

the fact that the required APRM was inadvertently bypassed. The inspectors reviewed

entries in the Unit 2 unit supervisor's logbook and determined that no other APRM

18

C.

channel was inoperable or bypassed at the time of this incident and therefore the

licensee met TS requirements ..

Conclusions

Failure to follow procedures resulted in generation of an unexpected half-scram. That

action also resulted in disabling a reactor core protective feature without operators

being knowledgeable of the situation. A licensee established barrier, independent

verification, failed to prevent this event.

M4.2

Maintenance Refuel Floor Activities Result in Unexpected Main Control Room Alarm

a.

Inspection Scope

The inspectors reviewed the circumstances associated with poor work practices on the

refuel floor that resulted in receipt of a main control room annunciator.

b.

Observations and Findings

On August 5, 1998, licensee and contractor personnel were performing fuel pool

cleanup activities in the Unit 3 fuel pool. Part of the cleanup activities included the use

of a water lance to flush underwater cutting equipment. When workers left the refuel

floor for lunch, they inadvertently left the water supply used for the cleaning activities

turned on. With the water supply left running, level in the fuel pool started to rise and

eventually caused the high water level alarm in the main control room to annunciate.

Operators correctly responded to the alarm in accordance with the annunciator

. response procedures. Refuel floor personnel were informed of the fuel pool high level

alarm, the water input to the pool was secured, and all work stopped on the refuel floor.

Operators successfully lowered fuel pool level back to normal and no adverse safety

consequences occurred as a result of the incident.

The licensee documented the occurrence via Problem Identification Form 01998-0467 4

and initiated a prompt investigation. The licensee implemented corrective actions to

address the issue including management discussion of refuel floor activities at the daily

plan of the day meeting to ensure that all managers would be aware of future refuel'

floor activities.

c.

Conclusions

The operators responded well to this self-revealing, emergent event. The poor work

practices on the refuel floor presented an unnecessary challenge to control room

. operators.

MB

Miscellaneous Maintenance Issues

M8.1

(Closed) Unresolved Item 50-237/249-97003-02: Corrective actions concerning torus

pitting. ComEd stated by Letter JSPLTR #97-0066 dated April 2, 1997, that although

grinding of pits to provide a 4:1 taper was not performed as originally specified, the pits

19

E1

E1.1

ES

E8.1

were considered acceptable. The inspectors reviewed and concurred with the

licensee's engineering evaluation, which supported the conclusion that the pits were

acceptable. The inspectors reviewed Work Packages 004014 and 010177 and

verified that recoating of the pits had been performed to hinder further corrosion. The

inspectors also reviewed work scheduling documentation to confirm that the licensee

scheduled torus inspections, including inspection of underwater portions, for each

refueling outage and that the licensee scheduled corrective actions in response to

March 1998 torus inspection findings. This item is closed.

Ill. Engineering

Conduct of Engineering

Effectiveness of Licensee Corrective Actions for Past Problems

The inspectors reviewed licensee corrective actions associated with older, historical

problems at the station (reference Section ES, "Miscellaneous Engineering Issues").

Some of the older outstanding problems at the station are similar to current problems

experienced by the station that are documented in recent NRC inspection reports.

Examples included HPCI system material condition deficiencies, off-gas system fires,

and reactor vessel post-scram overfill problems due to inadequacies associated with

the feed water level control system. The inspectors closed these issues because the

older items were enveloped by newer, current inspection followup items. While the

licensee ha*s made progress in resolving old concerns, and the current issues are not

as severe as the older items, the repetitiveness of several of the items indicated that

licensee corrective actions had not always been effective at eliminating the concerns.

Miscellaneous Engineering Issues

(Closed} Unresolved Item 50-237/249-94014-04: The failure of the High Pressure

  • Coolant Injection System 2-2300-05 valve to perform its intended safety function when

required by an automatic *initiation signal and the concern over the quality of the

ongoing investigation. The licensee subsequently submitted LER 94024,

Docket 50-237, "HPCI Outboard Containment lsoJation Valve Failure to Close due to

Corroded Contacts in Local Push Button Station"; this report discusses the LER ..

Report 94014 also described an instance of a failure to perform a 50.59 evaluation on

the support stand for the local controller of the HPCI outboard containment isolation

valve. The licensee could not find any 1994 tracking items for failing to perform an

evaluation of the support stand. Licensee engineers walked down the support and

determined that it was currently adequate, but the engineers were unable to locate any

supporting calculations. Ori July 28, 1998, the licensee initiated PIF# 01998-04561 to

enter the apparent lack of a 50.59 evaluation into the corrective actions process, and*

subsequently assigned NTS Item 23720198357501 with a due date of October 2, 1998,

to address the 50.59 screening. This unresolved item is closed.

. 20

EB.2

{Closed) Inspection Followup Items (I Fis) 50-237 /249-94016-01. 50-237 /249-94016-04.

50-237/249-94016-05. 50-237/249-94016-06. 50-237/249-94016-07; Weak Design

Calculation Control: The above items were all items from the System Based Instrument

and Control Inspection (SBICI).

The following statement was included in the SBICI team report for each of the above

I Fis.

"Based on other margins identified in the calculation, the team concluded the above

items would not affect operability, however, these items represent another example of

weak design calculation control."

The inspectors reviewed the corrective actions taken for the weak design calculation

control. The licensee stated that from 1994 to 1996, Dresden was part of a program to

obtain all the design basis and calculations from the Architectural Engineering and

Design Groups for the plants. The licensee has now stored the calculation data basis

in the Electronic Work Control System (EWCS) Controlled Documents for Calcuiations.

The documents were available as necessary to plant personnel on a read only bases.

Selected clerks accomplished changes to the information.

The licensee has entered all the calculations for the plant into the EWCS, which may

be read or printed by anyone with access to the data base. This issue is closed.

EB.3

{Closed) Unresolved Item 50-237/249-96002-11: Resolution of NRG-identified Updated

Final Safety Analysis Report (UFSAR) issues. This unresolved item involved NRC-

identified discrepancies in information in the UFSAR regarding the following items:

containment locked valve status, diesel fuel oil storage tank overflow, ACAD system

status, toxic gas analyzer, and differences between condensate storage tanks A and B

relative to the HPCI system's dedicated suction. Report 96004 added an additional

discrepancy between the UFSAR and the diesel generator fuel oil day tank to this item.

The item was open pending review of the licensee's corrective actions.

These discrepancies reflected a historical lack of emphasis on maintaining the UFSAR.

The licensee acknowledged this weakness and implemented actions to assure proper

maintenance of the UFSAR. This item is now closed. Note that the following actions

addressed the specific issues of URI 96002-11:

21

Issue

Resolution and Significance

Incorrect Containment Locked Valve

50-person team rewrote and re-verified

Status

locked valve checklists. Violation 50-237;

50-249/96004-02 issued for corrective

actions associated with locked valve status.

Diesel Fuel Oil Storage Tank

UFSAR modified. This UFSAR error was

Overflow

considered minor.

ACAD System Status

UFSAR modified. This UFSAR error was

considered minor.

Toxic Gas Analyzer

Emergency Operating Procedures revised.

LER 237 96-003, "Main Control Room HVAC

Outside of Design Basis due to Inadequate

Implementation of Modification" issued.

This UFSAR error was tracked under the

LER.*

CST A and CST B HPCI Dedicated

UFSAR modified. This UFSAR error was

Suction differences

considered minor because annunciators and

alarms provided administrative control of

suction.

E8.4

{Closed) Unresolved Item 50-237/249-96004-06: Status of Safety Systems During

Valve Stroke Tests. This unresolved item was to.evaluate the acceptability of not

declaring emergency core cooling systems (ECCS) inoperable during motor operated

valve stroke tests. The concern was that the valves took longer to return to their safety

position than the safety analysis assumed for the ECCS to operate post-accident. The

licensee evaluated the concern and determined that declaring the systems inoperable

during stroke time testing was more feasible than redoing the safety analysis to .

account for the longer stroke times. The licensee accordingly altered the surveillance

procedures to reflect this position. This item is closed.

.E8.5

E8.6

(Closed) Unresolved Item 50-237/249-96004-07: Weak Justification for Environmental

Qualification of Pressure Controller. The licensee reperformed the calculation to

support operability of the controller in the post-accident environment. This item is

closed.

{Closed) Inspection Followup Item 50-249/96006-02: Thirty-day Special Report:

Inoperable Recombiners Due to Short Duration Off Gas System Fires. The licensee

implemented a number of corrective actions in response to short duration off gas

system fires in 1995. These actions were not completely effective, as evidenced by the

occurrence of fires in the 3A off Gas train on December 6, 1997, and January 13, 1998,

(reference IR 50-237/249-97028(DRP)). The licensee assigned multiple nuclear

tracking system items to track and implement improvements to the off gas system. The

22

NRG will review these actions as part of routine resident core inspections. This item is

closed.

EB.7

(Closed) Unresolved Item 50-237/249-96006-10: The reactor building ventilation

system did not meet the flow values listed on Updated Final Safety Analysis Report

.(UFSAR), Figure 9.4-15. This issue was open pending the inspectors' review of the

licensee's evaluation. The written response provided to the inspectors stated that the

licensee did not intend to make the "Information Only" drawings part of the design basis

of the plant. Section 1. 7, "Drawings and other Detailed Information," of the UFSAR *

also stated "Selected P&IDs shown in the UFSAR are for information only."

The licensee researched the issue in 1996 and found no references to specific flow

values in the text. The licensee also reviewed the original GE design and found that

references to air flow were only coupled to maintaining reactor building temperatures.

The licensee determined that, as described in text of the UFSAR, the design basis for

the ventilation system was to maintain reactor building temperatures, to provided at

least one free-volume change per hour, and to maintain at least-1/4" differential

pressure (dp) within the reactor building, and at least -1/4" dp between clean and

potentially contaminated areas.

During the current inspection period, the inspectors requested that the licensee show

how the reactor building ventilation system met the design basis determined in 1996.

The system engineer informed the inspectors that no tests or calculations existed to

show that the system met its design basis. The inspector asked if there were any plans*

to change the UFSAR, and the system engineer responded that there were none.

The inspectors were concerned that the licensee had not shown that the plant was

within compliance with the UFSAR despite the two years since the inspectors raised the

original concern. The inspectors discussed the issue with the plant management, and

the licensee subsequently performed tests and concluded that the reactor building

ventilation could exchange two volumes per hour.

The original unresolved item was a concern that the UFSAR design basis of the reactor

building ventilation system was shown on UFSAR Figure 9.4-15. The ability of the

system to meet the flow rates shown on the drawing was the crux of the concern.

Figure 9.4-15 was a photocopy of Critical Drawing M-269 Rev Q, "Diagram of Reactor

Building Ventilation," and was labeled "For Information Only." The inspectors noted

that Figure 9.4-15 was also marked, "This drawing is superseded by M-269, Sh. 1 & 2,"

Drawings M-269, Sheets 1 and 2 were not part of the UFSAR.

Paragraph 71(e) of 10 CFR Part 50 states that the UFSAR shall be revised to include

changes made in the facility. The inspectors were concerned that the use of

superseded "information only" drawings in the UFSAR may not comply with

. 10 CFR 50.71(e). The original Unresolved Item 50-237/249-96006-10 is closed.

However, the overall use of "information only" drawings as described in UFSAR

Section 1.7, is considered unresolved pending the inspector's review of the issue with

the office of Nuclear Reactor Regulation (URI 50_-237/249-98021-03(DRP)) .

23

.J

E8.8

(Closed) Unresolved Item 50-237/249-97013-06(DRP)}: 250 VDC Battery Loading.

This item was open pending further NRC review of the UFSAR, the licensee's response

to the NRC Independent Safety Inspection Report, and the revised battery calculation.

The licensee identified on August 12, 1997, that the last TS battery load profile

surveillance test did not use the worst-case load profile. Revision 11, of the battery

  • loading calculation (PMED 898230-01) had the same error. The worst-case profile only

existed when the licensee aligned a unit to the swing charger, and the same unit

powered the swing charger, and the 2/3 emergency diesel generator tripped.

Previously, the licensee had based the worst-case profile on having the Unit 2(3)

charger in service ~nd the Unit 2(3) diesel tripping. At Dresden, the 2/3 swing charger

is a spare charger, and not normally in use. This item was open pending further NRC

review of the UFSAR, the licensee's response to the NRC Independent Safety

Inspection Report, and the revised battery calculation.

As corrective action to the error, the licensee revised the battery and charger alignment

procedures to prevent the worst case scenario by prohibiting aligning the 2/3 swing

charger to the same unit from which the charger was energized. This prohibition made

the previously analyzed trip of the Unit 2(3) diesel bounding.

The initial discovery of the new worst-case scenario was determined by the licensee not

to be reportable to the NRC. During review of this unresolved item, the inspectors

requested that the licensee confirm this decision. The licensee concluded that the

event was reportable and commenced making a LER. The inspectors will review this

issue, along with the timeliness of the reporting of the event to the NRC, after receipt of

the LER.

This unresolved item is closed.

E8.9

(Closed) URI 50-237/249-98007-04: Concern that a lake hot canal dike failure might .

lower the plant intake canal water level to below the 495' Mean Sea Level (MSL)

analyzed in the UFSAR. ComEd responded to this URI by docketed letter dated

June 25, 1998, and stated that the lowest elevations of all connections of the lake hot

and cold canals to the Units 2 and 3 intake and discharge canals were at 496' MSL.

Therefore, failure of the lake canal dikes could not lower the intake and discharge canal

water levels to less than 495' MSL. The inspectorreviewed Sheets 1 and 2 of the

Circulating Water Flumes - Plan and Profile Drawings (S-17 and S-18), which indicated

that the lowest elevations of the lake hot and cold canal connections to the intake and

discharge canals were at 496' MSL. The inspector determined that any lake canal dike

failure was properly bounded by the Dresden Dam failure UFSAR analysis. This item is

closed .

24

E8.1 O (Closed) LER 50-237/94024-00: HPCI Outboard Containment Isolation Valve Failure to

Close due to Corroded Contacts in Local Push Button Station .

On August 4, 1994, Unit 2 was at 99 percent of full power. The Unit 2 HPCI system

failed its monthly operating surveillance because one of the HPCI turbine exhaust

check valves failed closed. The HPCI system failure required the licensee to shut down

Unit2.

On August 9, 1994, during the shutdown for repairing the HPCI system, the Unit 2

HPCI system outboard containment isolation valve, 2-2301-5, should have closed when

reactor pressure dropped below 80 psig, but the valve failed to close automatically.

However, the inboard valve closed, so the HPCI system valves accomplished

containment isolation. The operators could not close the outboard valve by use of the

control room switches either, but the operators did eventually close the valve by use of

the local handwheel.

The licensee found that the valve's local control station push button contacts were

corroded. The corrosion made an open circuit that prevented operation of the valve.

The licensee cleaned the contacts on the HPCI system valve controller, and did the

same for about 130 other safety-related local controllers. Also, the licensee *

implemented an every-other-refueling maintenance task to clean the contacts.

The inspectors conducted a search for problems related to corroded contacts on local

valve controls, and the search showed no additional problems. The inspectors verified

that work documents showed that valves 2-2301-5 and 3-2301-5 had received

subsequent cleanings, and were currently cleaned. This LER is closed.

IV. Plant Support Areas

Radiological Protection and Chemistry (RP & C}

R4

Staff Knowledge and Performance in RP&C (RP & C}

R4.1

Release of Contaminated Material Off-Site

a.

Inspection Scope

On August 13, 1998, the licensee released a truckload of dirt offsite. The licensee

subsequently sampled the dirt and two of the four samples exceeded the licensee's

radiological criteria for free-release of material from the station.

b.

Observation and Findings

On August 13, 1998, the licensee performed excavating to support repairs on an

underground storm sewer. The licensee was performing the work in a non

radiologically controlled area of the site. A contract radiation protection technician

25

associated with Unit 1 was overseeing the work and did not perform the sampling

required for a full unconditional. release of the material.

Consequently, the licensee released a truck filled with dirt from the excavation from the

site. On August 14, 1998, the licensee filled a second truck with dirt from the job.

Utility radiation protection personnel observed the job and questioned why licensee

personnel did not take isotopic analysis samples before releasing the material. At that

point, the licensee identified that a truck was released the prior day without the

performance of the required isotopic analysis. The utility then performed an isotopic

analysis of the dirt that had already been released from the site. Two of the four

samples indicated levels of Cesium-137 that were just above the licensee's free release

  • criteria. The licensee collected the material and returned it to the site.

The licensee documented the occurrence via PIF 01998-04836. The licensee informed

the inspectors that a full root cause analysis would be performed to determine how

barriers broke down to allow the material to be released: The radiological

consequences of the event were minor. The inspectors will review the root cause

analysis during routine resident and regional plant support inspection activities.

c.

Conclusions

X1

While the radiological consequences of the event were minor, breakdowns in licensee

processes and practices resulted in the release of contaminated soil from the site. *

V. Ma~agement Meetings

Exit Meeting Summary

The inspectors presented the inspection results to members of license management at

the conclusion of the inspection on August 25, 1998. The licensee acknowledged the

findings presented. The inspectors asked the licensee whether any materials

examined during the inspection should be considered proprietary. No proprietary

information was identified .

26

"

Partial List of Persons Contacted

Licensee

L. Aldrich, Radiation Protection Manager

J. Almon, Training Manager

P. Boyle, Chemistry Department Head

S. Butterfield, Regulatory Assurance NRG Coordinator

P. Chabot, Engineering Manager

L. Coyle, Operations SOS

R. Fisher, Maintenance Manager

T. Fuhs, Regulatory Service, NLA

J. Harlach, Supervisor Service Manager

M. Heffley, Site Vice President

R. Kelly, Regulatory Assurance

W. Lipscomb, Site Vice President Staff

M. Milly, Supply Maintenance Department Head

M. Pacilio, Work Control and Outage Manager

F. Spangenberg, Regulatory Assurance Manager

S. Stiles, Nuclear Oversight Manager

P. Swafford, Station Manager

R. Weidner, Corrective Action Program Supervisor

K. Riemer, Senior Resident Inspector

D. Roth, Resident Inspector

B. Dickson, Resident Inspector

M. Ring, Chief Reactor Projects Branch 1

27

. "

I

List of Inspection Procedures Used

IP 62707:

IP 71707:

Maintenance Observations

Plant Operations

IP.71750:

IP 92903:

IP 92902:

Plant Support Activities

Followup - Engineering

Followup - Maintenance

List of Items Opened, Closed,. and Discussed

50-249-98021-01

50-237-98021-02

50-2371249-98021-03

Closed

237/249-94014-04

237/249-94016-01;

04; 05; 06; and 07

2371249-95009-02

2371249-95015-07

249-96006-02

237/249-96002-11

2371249-96004-06

2371249-96004-07

237/249-96006-10

2371249-97003-02

237197013-06

2371249-98007-04

237-90002-02

237-9500,1-01

237-95006-00

237-95013-00

237-95015-00&01

VIO

Violation of TS 3.8.D "Control Room Emergency

Ventilation.

VIO

Failure to Follow Procedures

URI

Use of "Information Only" drawings as described in

UFSAR Section 1.7.

URI

IFI

IFI

URI

IFI

URI

URI

URI

URI

URI

URI

URI

LER

LER

'

LER

LER

LER

Failure of HPCI System Valve to Perform its Intended

Safety Function

Weak Design Calculation Control

OOS and Equipment Configuration Control Problems

Drawing Error

Thirty-day Special Report: Inoperable Recombiners

Resolution of NRC-ldentified UFSAR Issues

Status of Safety Systems During Valve Stroke Tests.

Weak Justification for Environmental Qualification of

Pressure Controller

Reactor Building Ventilation System did not Meet Flow

Values on FSAR

Corrective Actions Concerning Torus Pitting

250 VDC Battery Loading

Concern That a Lake Hot Canal Dike Failure Might Lower

Plant Intake Canal. Water Level

Reactor Scram Following Condensate/Condensate

Booster Pump Failure due to Internal Failure

Scram From Main Turbine Stop Valve Closure Due to

Moisture Separator Level High High

TIP System Isolation Does Not Have "Seal in"Logic on

Group II Isolation

.

Inadequate Sampling of Service Water Effluent Due to

Use of a Superseded Procedure and Recent System

Configuration Change

Leakage Limit Exceeded Due to Excessive Leakage Past

MSIV

28

j

237-95017-00

LER

Containment Cooling Service Water Vault Penetration

Seals Failed Leak Test Due to Being Out of Adjustment

249-95008-01

LER

Scram From Main Turbine Stop Naive Closure Due to

Turbine Trip on High Vibration

249-95010-00

LER

Inadequate LCO Entry Due to Inadequate Control of

Decay Heat During Cooldown

237-94024-00

LER

HPCI Outboard Containment Isolation Valve Failure to

Close

237-97013~00

LER

HighPressure Coolant Injection System Inoperable Due to

Excessive Cycling of the Gland Seal Condenser Drain

Pump Due to Level Switch Malfunction.

249-97-014-00

LER

High Pressure Coolant Injection System Inoperable Due to

Gland Seal Leakoff Condenser Drain Pump Low Level

Shut Off Switch Failure Caused by a Misaligned Switch

Lever Arm.

249-98001-00

LER

High Pressure Coolant Injection System Inoperable Due to

Gland Seal Leakoff Condenser level Control Malfunction

Caused by a Loose LLJg on the Drain Pump Automatic

Start Relay.

249-98-002-00

LER

High Pressure Coolant Injection System Inoperable Due to

Gland Seal Leakoff Condenser level Control Malfunction

from a Drain Pump Start Level Switch Failure Cause by

Original by Original Design Deficiency.

237-9.8-009-00

LER

High Pressure Coolant Injection System Inoperable Due to

Gland Seal Leakoff Condenser Level Control Malfunction

from a Drain Pump Start Level Switch Failure Caused by

Manufacturer Design Deficiency.

Discussed

None

29

ACAD

ACE

APRM

ccsw

CFR

CST

OAP

DATR

DIS

DOA

DOS

dp

DTS

ECCS

EOG

EPN

EWCS

HPCI

HVAC

IFI

IMO

IR

LCO

LER

LPCI

MEL

MSIV

MSL

NCAD

NSO

NTS

oos

PAM

P&ID

PIF

PORC

RCU

RG

RPS

TIP

TS

TSC

UFSAR

URI

LIST OF ACRONYMS USED

Atmospheric Containment Atmosphere Dilution

Apparent Cause Evaluation

Average Power Range Monitor

Containment Cooling Service Water

Code of Federal Regulations

Condensate Storage Tank

Dresden Administrative Procedure

Dresden Administrative Technical Requirements

Dresden Instrument Surveillance

Dresden Operating Abnormal

Dresden Operations Surveillance

Differential Pressure

Dresden Technical Surveillance

Emergency Core Cooling System

Emergency Diesel Generator

  • Electronic Part Number

Electronic Work Control System

High Pressure Coolant Injection

Heating Ventilation and Air Conditioning

Inspector Followup Item

Instrument Maintenance Department

Inspection Report

Limiting Condition for Operation

Licensee Event Report

Low Pressure Coolant Injection

Master Equipment List

Main Steam Isolation Valve

Mean Sea Level

Nitrogen Containment Atmosphere Dilution

Nuclear Station Operator

Nuclear Tracking System

Out-of-Service

Post-Accident Monitoring

Piping and Instrument Drawing

Problem Identification Form

Plant On-site Review Committee

Refrigeration Cooling Unit

Regulatory Guide

Reactor Protection System

Traversing In-Core Probe

Technical Specification

Technical Support Center

Updated Final Safety Analysis Report

Unresolved Item

30