ML17180A549

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Insp Repts 50-237/93-29 & 50-249/93-29 on 931007-1129. Violations Noted.Major Areas Inspected:Maint & Surveillance Observations,Engineering & Technical Support Observations & Plant Support
ML17180A549
Person / Time
Site: Dresden  
Issue date: 12/16/1993
From: Hiland P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17180A547 List:
References
50-237-93-29, 50-249-93-29, NUDOCS 9312280101
Download: ML17180A549 (21)


See also: IR 05000237/1993029

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION I I I

Repbrt Nos. 50-237/93029(DRP); 50-249/93029(DRP)

Docket Nos. 50-237; 50-249

License Nos. DPR-19; DPR-25

Licensee:

Commonwealth Edison Company

Opus West III

1400 Opus Place - Suite 300

Downers Grove, IL

60515

Facility Name:

Dresden Nuclear Power Station, Units 2 and 3

Inspection At:

Morris, IL

Inspection Conducted: October 7 through November 29, 1993

Inspectors:

M. Leach

A. M. Stone

M. Peck

R. Landsman

D. Chyu

R. Roton

G. Hausman

R. Zuffa, Illinois Department of Nuclear Safety

Approved By: f~c1-1lLI

i..//~ /q J

P. L. Hiland, Chief

Reactor Projects Section 18

Inspection Summary

Inspection from October 7 through November 29. 1993 (Report Nos.

50-237/93029(0RP); 50-249/93029(DRP))

Date

Areas Inspected: Routine, unannounced resident inspection of operations,

operational safety verification and engineered safety feature (ESF) system

walkdown, maintenance and surveillance observations, engineering and technical

support observations, plant support observations, safety assessment and

quality verification, licensee action on previous inspection findings,

licensee event report review, and management meetings.

Results: Of the nine areas inspected, one violation concerning failure to pos:

a Notice of Violation was identified in paragraph 6.

Two unresolved items

regarding disconnected drywell

ventilatio~ duct supports and missing main

steam line isolation valve seal assemblies were identified in paragraphs 3.e

and 4.a, respectively .

9312280101 931216

~

PDR

ADOCK 05000237.

G

PDR

EXECUTIVE SUMMARY

Assessment of Plant Operations

Operations continued to control unique activities very well, such as Unit 2

shutdown and startup.

One exception was the level of senior reactor operator

involvement in the approach to criticality. Personnel errors continued to

affect plant operations.

Errors involving supervisors were of particular

concern.

Operations closeout of the Unit 2 drywell was better than previous

occasions.

However, the general cleanliness level in Unit 2 drywell was below

management expectations.

Assessment of Maintenance and Surveillance

Observed maintenance and test activities were performed well.

However, low

priority work requests had the same average age as higher priority items and

the number of safety related work items increased.

Assessment of Engineering and Technical Support

Engineering performed a good review of the modification to the reactor vessel

water level instrument and identified an unreviewed safety question.

Assessment of Plant Support

The licensee failed to post a Notice of Violation within the required time

period .

2

1.

DETAILS

Persons Contacted

Commonwealth Edison Company CCECo)

M. Lyster, Site Vice President

G. Spedl, Manager, Dresden Station

D. Ambler, Executive Assistant to the Site Vice President

E. Carroll, Chemistry Supervisor

R. Flahive, Technical Services Superintendent

L. Jordan, Health Physics Supervisor

M. Korchynsky, Senior Operating Engineer

J. Kotowski, Operations Manager

  • G. Kusnik, Quality Control Supervisor
  • S. Lawson, Operating Engineer
  • H. Massin, Manager, Station Engineering and Construction

T. O'Connor, Maintenance Superintendent

  • R. Radtke, Services Superintendent

S. Reece-Koenig, Performance Assistant Administrator

  • R. Robey, Director, Site Quality Verification
  • J. Shields, Regulatory Assurance Supervisor

R. Speroff, Operating Engineer

R. Stobert, Operating Engineer

  • M. Strait, Technical Staff Supervisor

B. Viehl, Modification Design Supervisor

  • J. Williams, Operations Support Supervisor

R. Wroblewski, NRC Coordinator

  • Indicates persons present at the exit interview on November 29, 1993.

The inspectors also contacted other licensee personnel including members

of the operating, maintenance, security, and engineering staff.

2;

Summary of Operations

Unit 2

Unit 2 power level was administratively derated 1% power due to

feedwater flow nozzle calibration uncertainties.

On October 26, the

reactor was placed in the shutdown mode for a planned 3-day outage to

repair two traversing incore probes.

On October 30, the 2A and lD main steam isolation valves (MSIV) failed a

local leak rate test and required replacement of the seat ring.

The

  • outage was extended to facilitate the repair. Also, the licensee

identified an air leak on the 18 MSIV and determined that the

manufacturer had not installed air side seal assemblies in all eight

MSIV actuators.

Unit 2 was made critical on November 28 and synchronized to the grid on

November 29.

3

. \\

Unit 3

Unit 3 operated at power levels up to 99% for most of the period.

The

unit was derated 1% power due to feedwater flow nozzle calibration

uncertainties.

On November 4, the unit began coastdown in preparation

of the March 1994 refueling outage.

No violations or deviations were identified.

3.

Plant Operations (71707, 71710, and 93702)

The inspectors verified that the facility was operated in conformance

with the licenses and regulatory requirements and that the licensee's

management control system was effectively carrying out its

responsibilities for safe operation. During tours of accessible areas

of the plant, the inspectors made note of general plant and equipment

conditions, including control of activities in progress.

On a sampling basis, the inspectors observed control room staffing and

coordination of plant activities, observed operator adherence with

procedures and technical specifications, monitored control room

indications for abnormalities, verified that electrical power was

available, and observed the frequency of plant and control room visits

by station managers.

The inspectors also monitored various

administrative and operating records .

Accessible portions of ESF systems and associated support components

were inspected to verify operability through ooservation of

instrumentation and proper valve and electrical power alignment.

The

inspectors also visually inspected components for material condition.

Specifically, the following systems were inspected by direct field

observations:

Unit 2

Reactor protection system relays and components

Suppression pool cooling system

2/3 diesel generator

ATWS logic and relay system

Diesel generator

Unit 3

Reactor protection system relays and components

ATWS logic and relay system

Diesel generator

4

Plant Operations Observations

a.

Personnel Errors

A number of significant personnel errors occurred during the

period.

The following provides a summary of the events:

On October 13, an operator failed to wear required

protective clothing for a task in the 34 kv switchyard,

opened the wrong disconnect, and then re-closed the

disconnect without direction.

On October 26, an operator removed Unit 3 offgas filter

train from service instead of Unit 2 train. The operator

failed to self-check.

On October 30, while removing cable from Unit 2 drywell, a

supervisor incorrectly cut a cable for the "B" traversing

incore probe indexer.

On November 8, an electrical mechanic (EM) inadvertently

tripped the 38 fuel pool cooling pump.

The EM was

troubleshooting the 3A pump and worked on the wrong mercury

switch.

On November 9, Unit 3 ECCS jockey pump was found running

with the suction, discharge, and recirculation valves

closed.

The pump had been incorrectly returned to service

earlier in the day. A supervisor had decided not to use the

procedure for this task.

On November 11, a station laborer supervisor directed two

laborers to hang hoses and cable more than 6 feet above

ground.

The required radiological survey was not obtained.

On November 16, instrument maintenance personnel worked on

the incorrect local power range monitor and caused a channel

"A" half scram on Unit 2.

On November 16, while clearing an out-of-service (OOS) for

work on the service air compressors, operators found four

valves open.

As stated on the OOS cards, these valves were

required to be closed.

The initial investigation suggested

that contractors had opened the .valves.

These events demonstrated a continuing problem with licensee

personnel attention to detail and procedural adherence.

The

involvement of first line supervision in three of these events

5

-1

b.

c .

demonstrated that upper management expectations have not reached

the lower levels of supervision. Therefore, first line

supervision was unlikely to set the appropriate standards for the

bargaining unit personnel.

The event involving the high voltage operator in the 34 kV

switchyard showed a disregard for electrical safety as well as a

failure to self check.

The involvement of a trainee in this event

also showed a failure to establish the correct standards for

future operators.

In addition, specific corrective actions for

this event have been slow.

A number of enforcement actions have been taken in the past with.

regards to procedural adherence at Dresden station. The

corrective actions for the most*recent Notice of Violation (50-

237/93020-01) have not yet had sufficient time to be implemented.

Therefore, the above personnel errors are considered further

examples of this violation.

Observations During Unit 2 Shutdown and Startup

The inspectors monitored activities of control room operators and

other operations support personnel during the Unit 2 shutdown on

October 25 and startup on November 28.

Management expectations,

with one exception, were clearly communicated to the operating

crews prior to both activities. The operators were attentive to

the panels and all observed activities were conducted in

accordance with plant procedures.

Discrepancies such as

intermediate range monitor 14 problems were identified and

resolved promptly.

The startup activities were conservatively

controlled with the nuclear engineers and the nuclear station

operators communicating effectively. The pre-job briefing by the

nuclear engineers and the shift control room engineer (SCRE) was

complete, with opportunity for input and questions from personnel.

The inspectors raised a question of senior reactor operator (SRO)

involvement during reactor startup at the beginning of 1993.

Licensee management stated a SRO should devote a majority of

oversight to the startup (Inspection Report 50-237/92036) and the

inspectors considered the lack of management direction to the

operating crews to be a weakness.

On November 28 during rod

withdrawal to criticality, there was no direct involvement by a

SRO.

Both the shift engineer and the SCRE periodically monitored

the startup activities. There was no formal communications to the

SROs on the status of the startup from either the nuclear

engineers or the nuclear station operators.

The level of

involvement of the SROs in reactor startups remained a weakness

and is considered an Inspector Followup Item (50-237/93029-

0l(DRP)).

Operator Response to Unit 3 Electro-Hydraulic Control Problems

6

d.

e.

On October 27, the operators received an electro-hydraulic control

electrical malfunction annunciator and initiated a work request.

The instrument maintenance foreman observed the 24 Vdc power

supply to the turbine supervisory controls was at 22 Vdc.

On

October 28, the foreman noted that the voltage had decreased below

20 Vdc.

The operating engineer immediately authorized a power

reduction to 40% power to prevent a potential reactor trip from a

turbine trip. The inspectors observed the power reduction and

verified the operators were aware of the potential reactor trip

condition.

The inspectors had no concerns.

Operations Involvement in Bus 29 Maintenance Work

On November 10, the inspectors observed operations involvement

with the safety related Bus 29 maintenance troubleshooting.

The

troubleshooting activities rendered several safety related systems

inoperable: high pressure coolant injection, one train of core

spray and low pressure coolant injection, Unit 2 diesel generator

cooling water, and Unit 2/3 diesel continuous lubrication pumps.

The licensee installed a temporary alteration to maintain

operability of the Unit 2/3 diesel generator continuous

lubrication pumps through a Unit 3 motor control center.

The

inspectors verified equipment status, compliance with technical

specifications, system lineups, and equipment tagouts.

No

problems were identified. The heightened level of awareness

meeting for restoration of equipment was very good and resulted in

good communication and coordination between all departments.

The

operations foreman identified a potential concern with breaker

operability and halted further work until the concern was

resolved.

The inspectors had no concerns.

Unit 2 Drywell Closeout

The inspectors accompanied licensee personnel on a Unit 2 drywell

closeout inspection.

The operations department improved in the

ability of finding debris than previous closeouts.

However, the

cleanliness standards for the drywell were lower than the

remainder of the plant; there were still many minor discrepancies.

The operations personnel removed significant quantities of duct

tape from the drywell.

This represented a weakness in the foreign

material exclusion program.

Improving drywell cleanliness with

due consideration for ALARA concerns is a challenge for the

licensee.

The inspectors identified two disconnected ventilation duct

supports in the drywell. This issue is considered an Unresolved

Item pending review of the licensee's evaluation (Unresolved Item

50-237/93029-02(DRP)).

Several examples of a previous violation for failure to follow

procedures were identified.

One inspector followup item was identified

concerning SRO involvement in reactor startup activities.

One

7

4.

unresolved item was identified regarding disconnected drywell

ventilation duct supports.

Monthly Maintenance and Surveillance (62703 and 61726)

Station maintenance and surveillance activities were observed and/or

reviewed to verify compliance with approved procedures, regulatory

guides, and industry codes or standards, and in conformance with

technical specifications (TS).

The following items were considered during this review: approvals were

obtained prior to initiating maintenance work or surveillance testing

and operability requirements were met during such activities, functional

testing and calibrations were performed prior to declaring the component

operable, discrepancies identified during the activities were resolved

prior to returning the component to service, quality control records

were maintained, and activities were accomplished by qualified

personnel.

The inspectors witnessed portions of the following maintenance

activities:

Unit 2

Troubleshooting of drywell equipment drain sump

Troubleshooting of Bus 29 to motor control centers 29-2 and 4

Repair of 28 control rod drive (CRD) motor

Replacement of 28.circulating water pump motor

Installation of reactor vessel level indication system (RVLIS)

modification

Replacement of service air compressor

Main steam isolation valves refurbishment

Replacement of 2A Reactor recirculation pump lower guide bearing

HPCI turning gear engagement mechanism modification

2/3 Diesel generator 18-month inspection

Unit 3

Installation of 250 Vdc balance-of-plant battery

Installation of fire protection system upgrade

Installation of non-outage piping for RVLIS modification

Installation of station blackout diesels and auxiliary equipment

3A CRD pump reducing gear rebuild

38 Circulating water pump

The inspectors also witnessed sections of the following test activities:

Unit 2

SP 91-10-134 Triennial Fire Main Yard Loop Flow Test

SP 93-3-32 Differential Pressure Testing of MO 2-1501-138

SP 93-3-101 Differential Pressure Testing of MO 2-1501-208

8

DIS 0700-08 Rod Block Monitor Calibration and Functional Test

DIS 1400-06 Core Spray Flow Transmitter Calibration

DOS 0250-02 Closure Timing and Exercising of Main Steam Isolation Valves

DOS 1400-01 Core Spray System Valve Operability Test

DOS 1400-02 Core Spray System Full Flow Test

DOS 1500-06 Low Pressure Coolant Injection System Full Flow Test

DOS 2300-03 High Pressure Coolant Injection System Full Flow Test

Unit 3

DIS 0500-10 Scram Discharge Volume Level Instrumentation Functional Test

and Calibration

DOS 0250-06 ADS Acoustic Monitor Surveillance

DOS 1400-01 Core Spray Pump Test with Torus Available

DOS 1400-05 Core Spray Valve Operability Test

DOS 1500-02 CCSW In-Service Pump Test

DOS 1500-03 CCSW Pump Test

DOS 1500-05 LPCI System Quarterly Flow Rate Test

DOS 1500-10 LPCI Quarterly In-Service Pump Test

Maintenance and Surveillance Observations

a.

Seal Assembly Missing from Main Steam Isolation Valve Actuator

On November 8, a maintenance foreman discovered an air leak on

Unit 2 lA and 28 main steam isolation valve (MSIV) actuators.

The

leakage was past the weep hole on the air side of the operator.

Upon disassembly, the licensee determined the air side seal

assembly had not been installed by the manufacturer, Miller Fluid

Power.

The licensee had ordered 17 actuators in 1991.

Eight of

these were installed in Unit 2 and five were installed in Unit 3

during previous refueling outages.

The licensee replaced the seal

assemblies on Unit 2 MSIVs during the recent forced outage.

The

licensee performed an engineering evaluation and concluded Unit 3

MSIVs were operable. Contingency actions included: raising the

minimum drywell pneumatic system pressure and revising operator

procedures to ensure operability during worst case accident

conditions.

The five Unit 3 actuators will be repaired during the

March 1994 refueling outage.

The inspectors had no concerns with

the operability evaluation.

The licensee's preliminary investigation indicated that the

actuators were designed by Commonwealth Edison Company and built

by Miller Fluid Power.

The double seal was designed in 1982;

however, appropriate design diagrams were not revised.

The root

cause for the missing seal assemblies and corrective actions are

considered an Unresolved Item (50-237/93029-03(DRP)) pending

review of the licensee's investigation .

9

. .

b .

c.

Maintenance Backlog

The maintenance staff has completed a review of the work request

backlog of currently available corrective maintenance items.

The

review showed some weaknesses in the work control and maintenance

programs:

Low priority work requests had the same average age as

higher priority work.

Although the total number of work requests had decreased,

the number of outstanding safety related work requests

continued to increase.

The systems with the largest number of outstanding work requests

were radwaste, ventilation, and some Unit 2 safety related and

important to safety systems. This was a concern because Unit 2

recently completed a major maintenance outage.

One example of failure to complete safety related work in a timely

manner was a work request on Unit 2 diesel generator.

Work

request 016676 involved two loose bolts on the diesel, was written

on March 5, 1993.

As of November 24, this item was not yet

scheduled for work.

Although the diesel generator remained

operable, this did not meet management's expectations for timely

corrective action.

The timeliness of maintenance activities will

be reviewed further in future inspections.

Replacement of Traversing Incore Probes

The inspectors observed the replacement of the traversing incore

probe detector tubing and the recovery of detector probes.

The

work was performed in accordance with WR 022322.

The pre-job

briefing was excellent.

Both health physics support and ALARA

planning considered various contingencies and precautions

associated with the evolution.

In addition, the instrument

maintenance staff performing the evolution was well coordinated,

enthusiastic, and precise.

No violations or deviations were identified.

One unresolved item was

identified regarding MSIV seal assemblies.

5.

Engineering and Technical Support (37700)

The inspectors evaluated the extent to which engineering principles and

evaluations were integrated into daily plant activities. This was

accomplished by assessing the technical staff involvement in non-routine

events, outage-related activities, and assigned TS s_urveillances;

observing on-going maintenance work and troubleshooting; and reviewing

deviation investigations and root cause determinations .

10

6 *

RVLIS Modification in Response to Bulletin 93-03

NRC Bulletin 93-03, "Resolution of Issues Related to Reactor Vessel

Water Level Instrumentation in Boiling Water Reactors," was issued on

May 28, 1993.

The bulletin alerted licensees of potential reactor water

level indication errors during normal depressurization.

The licensee's

immediate corrective actions were reviewed and were discussed in

Inspection Report 50-237/93017(DRP).

The long term corrective actions involved a modification to provide

continuous backfill through the instrument lines using control rod drive

(CRD) water.

Due to the system configuration, the licensee determined

the modification created an unreviewed safety question, in that, the

probability of a loss of coolant accident increased.

An inadvertent

closure of the reference leg root valve would cause the CRD water to

pressurize the instrument line and cause all relief valves to open.

The

licensee planned to implement administrative controls to prevent root

valve manipulation.

However, after further review by NRR, the licensee

was not granted permission to implement the modification.

The licensee

was reviewing possible design changes and planned to resubmit a proposed

design by early 1994.

No violations or deviations were identified.

Plant Support (71707 and 93702)

The inspectors evaluated the involvement of support organizations in

assuring safe and effective plant operation.

Specific areas included:

Radiation Protection Controls

The inspectors verified workers were following health physics

procedures and randomly examined radiation protection

instrumentation for operability and calibration.

An example of

failure to follow radiation protection procedures was discussed in

paragraph 3a.

Security

The inspectors monitored the licensee's security program to ensure

that observed actions were being implemented according to the

approved security plan.

No discrepancies were identified.

Emergency Preparedness

The inspectors verified the operational readiness of the control

room technical support center and operation support center.

Non-

routine events were reviewed to ensure proper classification and

appropriate emergency management involvement .

11

7.

Housekeeping and Plant Cleanliness

The inspectors monitored the status of housekeeping and plant

cleanliness for fire protection and protection of safety related

equipment from intrusion of foreign material.

Posting Notice of Violation

On October 18, the licensee received a Notice of Violation, included in

Inspection Report 50-237/93022(DRSS), for a lack of procedures for

control of contaminated material. This Notice involving radiological

working conditions was not posted within 2 working days as required by

10 CFR 19.11. This Notice was not posted until October 26.

Failure to

post a Notice of Violation involving radiological working conditions

within the required period was a Violation of 10 CFR 19.11 (50-

237/93029-04).

One violation of 10 CFR 19.11 was identified.

Safety Assessment and Quality Verification (SAQV) (40500)

The effectiveness of management controls, verification and oversight

activities in the conduct of jobs observed during this inspection were

evaluated.

Management and supervisory meetings involving plant status

were attended to observe the coordination between departments.

The

results of licensee corrective action programs were routinely monitored

by attendance at meetings, discussion with plant staff, review of

deviation reports, and root cause evaluation reports.

SAOV Related Events

a.

Problem Identification Form (PIFl Review

The inspectors performed a review of the Integrated Reporting

Program, including approximately 20 PIFs, which were originated

during the first 6 months of 1993.

The licensee has commenced

trending causal factors; however, this information has not yet

been incorporated into the corrective action program.

In some

cases, the inspectors observed delays or omissions in submitting

PIFs.

Several weaknesses were observed from the sample of PIFs:

PIF 2-201-93-509 was written to document an adverse trend in

missed NRC commitments.

This PIF was closed by

incorporating it into another PIF, one which addressed some

specific service water system commitments.

The second PIF

did not address the generic concerns raised by the original

PIF .

12

b *

PIF 2-200-93-033 involved problems with using correct

procedure revisions and had an original due date of

February 26, 1993. This PIF due date had been revised seven

times and had a final due date of November 25.

On November 8, an electrical maintenance mechanic

inadvertently tripped the 38 fuel pool cooling pump.

An

entry in the Unit 3 operator logbook stated a PIF would be

written.

However, as of November 24, a PIF had not been

generated. After inspectors' prompting, the licensee

initiated a PIF for the event and a second PIF for the

failure to write a PIF initially.

An operator wrote a PIF on a Unit 3 green backlit

annunciator in October; however, the PIF was not tracked by

the integrated reporting system.

Regulatory assurance

personnel were unaware of the issue.

The operator initiated

another PIF for the concern.

A PIF was also generated to

determine why the original PIF was not included in the

system.

In October a radiation protection technician wrote a number

of PIFs.

These PIFs were not submitted to event screening

for 3 weeks.

Review of Safety Quality Verification Audit

The inspectors reviewed the safety quality verification (SQV)

audit, "License/Technical Specification Compliance and Corrective

Actions," conducted between July 7 and 19, 1993.

The audit

involved a team of five individuals and included conduct of

operations, technical specification interpretations, use of

temporary alterations, equipment status, procedural compliance,

effectiveness of corrective actions for NRC commitments, INPO

issues and corrective action requests (CARs), and corrective

actions for the September 1992 rod mispositioning event.

The inspectors observed the following:

A CAR was written on temporary alterations not reflected in

critical control room drawings.

The lack of critical

control room drawings control was identified by the NRC in

April 1993.

The licensee's corrective actions addressed

design control records, but did not consider temporary

alterations.

The effectiveness of the previous corrective

actions was not evaluated.

The audit did not identify problems with the corrective

actions taken for September 1992 rod mispositioning event.

During initial license examinations, NRC operator licensing

13

'

"

8.

examiners identified problems with job performance measures

on this issue.

The team observed only four surveillances in progress and

did not identify procedural adherence problems.

The team

reviewed 51 completed surveillances and identified

administrative related problems.

Only two equipment operators were observed during the

conduct of operations review.

The inspectors discussed the findings with the SQV supervisor.

The structure of the SQV audits has been modified to allow

auditors flexibility in performing audit activities.

Additionally, the audit periodicity was reduced from 3 months to 6

weeks.

The SQV department was also reorganized and increased by

three auditors.

The inspectors will review the effectiveness of

these changes in future inspections.

No violations or deviations were identified.

Licensee Actions on Previous Inspection Findings (92701 and 92702)

(Closed) Violation (50-237(249)/92009-03(DRP)): Failure to have

procedures to support engineering development and submittal of MDV

thrust calculation. The inspectors reviewed "Guideline for Determining

Target Thrust Windows" which incorporated requirements for documentation

of assumptions when generating target thrust windows.

This item is

closed.

(Closed) Violation (50-237(249)/92009-04CDRP)): Failure to perform an

adequate 10 CFR 50.59 evaluation for the installation of measuring and

test equipment under a temporary alteration.

The inspectors reviewed

Dresden Administrative Procedure (OAP) 10-2, "10 CFR 50.59 Review

Screenings and Safety Evaluations," which required completion of form

10-20, "Design Issues Worksheet" for each safety evaluation prepared.

This item is closed.

(Closed) Violation (50-237(249)/92009-05(DRP)): Failure to complete and

follow administrative procedures.

This item is closed to Violation 50-

237 /93020-01.

(Closed) Violation (50-237(249)/92009-06CDRPll: Failure to document

causes and corrective action taken for MDV non-conformance.

The

inspectors reviewed OAP 2-29, "Integrated Reporting Process" and CECo's

engineering and construction (ENC) integrated reporting program (IRP)

prescribed in ENC-QA-40.

Additionally, the inspectors sampled several

MDV related problem identification forms (PIFs) both from the station

and corporate office. The IRP appeared to provide a mechanism for

tracking issues and a systematic root cause evaluation method for non-

conformance.

This item is closed .

14

. ..

(Closed) Violation (50-237(249)/92009-07(DRP)): Failure to notify the

NRC of conditions that resulted in automatic actuation of engineered

safety feature.

The inspectors reviewed DAP 2-28, "Reportability

Determination and Event Notification 11 and the CECo Reportability

Manual.

This item is closed.

(Closed) Unresolved Item (237/90016-03(DRS); 249/90015-03(DRS)):

Neutron flux monitoring instrumentation did not meet Regulatory Guide

(RG) 1.97, Category 1 requirements. The Office of Nuclear Reactor

Regulation (NRR) completed an evaluation of the boiling water reactor

(BWR) owners group report, NED0-31558, "Position on NRC Regulatory Guide

1.97, Revision 3, Requirements for Post-Accident Neutron Monitoring

System.

11

NRR concluded that for current BWR license holders, the

NED0-31558 criteria was an acceptable alternative to* the recommendations

of RG 1.97.

NRR requested the licensees to review their neutron flux

monitoring instrumentation against the NEDD criteria and submit the

results of that review to NRR.

On August 17, 1993, the licensee

provided some of the requested information; however, the licensee stated

that further review would be required to assess the actions necessary to

comply with those NEDD recommendations not currently addressed by system

design.

The licensee stated that this information would be submitted to

NRR in 90 days.

No further Region III action is required. This item is

closed.

(Closed) Unresolved Item (50-237/91031-03 (DRP)): Division II, 480V

motor control center (MCC) main power feeder cables, located in the

turbine building, were run in Division I cable trays.

During Unit 2

cable walkdowns to resolve degraded voltage concerns, the licensee

identified four safety related cables that did not meet MCC feeder cable

separation requirements.

These cables were classified as balance-of-

plant during original plant construction. Several of the systems fed by

these cables were upgraded from non-safety to safety related after

Dresden received an operating license. The licensee indicated in the

safety assessment that the system upgrades were for future maintenance

and procurement purposes.

The licensee analyzed the potential failure mechanisms for each of the

identified cables.

The analysis included seismic, high energy line

break, internal and external missiles, and fire.

The licensee

determined that the most probable failure mechanism would be a fire.

The fire scenario was analyzed in the Dresden Appendix R Safe Shutdown

Report.

For the cables of concern and the fire areas they were located

in, systems and components from the opposite unit were available to

achieve and maintain safe shutdown.

Procedures were in place at the

time of discovery to mitigate this event.

The licensee has re-routed

the affected cables and now meets the divisional separation

requirements.

Unit 3 MCC safeguards cables were also walked down.

Two

cables were identified with the balance-of-plant segregation code.

However, divisional separation requirements were satisfied. This item

is closed .

15

. .

'

(Closed) Unresolved Item (50-237/92020-07 (DRP)): Apparent Rounds

Falsification. This item has been resolved through generic

communication to the industry. This item is closed.

(Closed) Unresolved Item (50-237/92026-03(DRP)): Loss of CCSW train

separation.

This issue was discussed in previous Inspection Reports

(50-237/93011, 93020, and 93024) and was the subject of Violation (50-

237/93024-03(DRP)).

This item is closed.

(Open) Inspector Followup Item (50-237/92005-01 (DRP)): Extended out-of-

service periods.

The operations department identified those components

with extended out-of-service periods.

System engineers were to review

these for possible modifications or other resolutions. This review did

not occur.

This item remains open.

(Closed) Inspector Followup Item (237/92010-0l(DRP)): Failure to perform

a 10 CFR 50.59 safety evaluation associated with the installation and

use of a portable containment air sample pump.

The inspectors reviewed

the licensee's procedure revisions and the rebaselining of the FSAR

section 5.2.2. This item is closed.

(Closed) Inspector Followup Item (249/92010-02(DRP)): Completion of

licensee initiatives to ensure against radioactive releases when using

the isolation condenser for extended time periods without offsite power.

The licensee's corrective actions included the installation of redundant

diesel driven clean demineralized water makeup pumps to supply makeup to

the isolation condenser shell side. These corrective actions were

either completed or planned for completion at the next refueling cycle.

This item is closed.

(Closed) Inspector Followup Item (50-237/92014-02(DRP)): Licensee

initiatives to improve performance and reduce engineered safety features

actuations associated with the reactor water cleanup (RWCU) system.

The

licensee performed various maintenance activities during last Unit 2

refuel outage.

The licensee planned to perform similar activities

during the next Unit 3 refuel outage. This item is closed.

(Closed) Inspector Followup Item (50-237(249)/92021-02(DRS)): Review of

modification package to eliminate noise in the neutron monitoring

system.

Modification package Pl2-2-92-726 was reviewed and found

acceptable. This item is closed.

(Closed) Inspector Followup Item (50-237/92036-03(DRP)): Elevated high

pressure coolant injection (HPCI) discharge piping temperature due to

reactor feedwater system back-leakage.

One outstanding corrective

action is the installation of a permanent temperature monitor on the

HPCI discharge piping.

The modification will be implemented during a

non-outage period in 1994.

This item is closed .

16

9.

(Closed) Inspector Followup Item (50-237/92036-04(DRP)): Reactor

automatic shutdown following condensate/condensate booster pump failure

and subsequent loss of offsite power.

The significant corrective

actions were completed.

This item is closed.

(Closed) Inspector Followup Item (50-237/92036-0SCDRP)): Manual reactor

shutdown due to feedwater oscillations during surveillance testing.

The

licensee implemented a modification which moved Unit 2 reactor vessel

level reference piping outside containment.

The Unit 3 modification is

scheduled for the next refuel outage.

This item is closed.

(Open) Inspector Followup Item (237/93017-03CDRP)): Incorrect positions

for Unit 2 drywell cooler dampers.

During the Unit 2 forced outage, the

licensee determined the 2D drywell fan was running backward.

The

discrepancy was not identified during the drywell ventilation walkdown

in May 1993.

The licensee's investigation into the root cause will be

evaluated with this inspector followup item.

This item remains open.

(Closed) Inspector Followup Item (50-237/93020-04(DRP)): 10 CFR 21

applicability for failed check valves.

The licensee submitted a 10 CFR

21 report on October 22, 1993.

The licensee identified ten C&S dual

disk check valves with viton seats. One has been replaced and the

remaining will be replaced when suitable valves are available. This

item is closed.

No deviations or violations were identified .

Licensee Event Reports (LERs) Followup (92700)

Through direct observations, discussions with licensee personnel, and

review of records, the following event reports were reviewed to

determine that reportability requirements were fulfilled, immediate

corrective action was accomplished, and corrective action to prevent

recurrence had been accomplished in accordance with technical

specifications.

(Closed) LER 237/89027. Revision 1: Postulated LPCI Swing Bus Loss

Resulting From Diesel Generator Voltage Regulator Failure Due to Design

Deficiency.

The licensee installed under/over voltage and frequency

protective relays. This LER is closed.

(Closed) LER 237/89029, Revision 4: Elevated HPCI Discharge Piping

Temperature.

This event was discussed in Inspector Followup Item (50-

237 /92036-03(DRP)).

This LER is closed.

(Closed) LER 237/91005, Revision 1: Orderly Shutdown Due to Leakage

Through Primary Containment Isolation Valves AO 2-220-44 and AO 2-220-

45.

This LER is closed.

17

. . .

(Closed) LER 237/91029: Main Steam Line Radiation Monitor Setpoints

Found Non-Conservative.

The remaining open action item involved a

possible technical specification change.

The licensee determined the

change was not necessary. This item is closed.

(Closed) LER 237/91-042, Revisions 0 and 1: Cable Separation Not Met.

This LER addresses the same topic as Unresolved Item 50-237/91031-

03(DRP), which was discussed earlier in this report. This LER is

closed.

(Closed) LER 237/92019: Containment Spray Interlock Momentarily

Inoperable Due to Surveillance Testing With the Unit 2/3 Diesel

Generator Inoperable.

The inspectors reviewed the procedure revisions

and the licensed operator training. This LER is closed.

(Closed) LER 237/92020: Unit 2 Reactor Vessel Exceeded Design Basis Due

to Non-Conservative Pressure/Temperature Curves.

This event was the

subject of a previous violation (50-237/92033-0l(DRP)).

This LER is

closed.

(Closed) LER 237/92032: Control Room HVAC Booster Fan Available Voltage

Less Than Required Minimum at Second Level Degraded Voltage Setting.

The licensee replaced the existing 100 volt-ampere (VA) control power

transformer with a 300 VA control power transformer and continued to

perform DOS 5750-1, "Control Room Standby HVAC Air Filtration* Unit

Surveillance," to verify operability. This LER is closed .

(Closed) LER 237/92037: Unit Emergency Bus Undervoltage Relay

Susceptible to Setpoint Drift Due to Design Deficiency.

Immediate

corrective action by the licensee was to modify the Asea Brown Boveri

Type 27N relays by removing the components susceptible to setpoint drift

and loss of time delay function due to elevated radiation dose during a

postulated loss of coolant accident and significant fuel failure.

The

time delay function was transferred to an agastat relay within the

system logic. Corrective actions to permanently resolve this issue will

be completed during the upcoming Unit 2 (D2R14) and Unit 3 (D3Rl3)

refuel outages. This LER is closed.

(Closed) LER 237/93007: ESF Actuation (ADS) Due to Simultaneous

Performance of LPCI and ADS Surveillance. The licensee revised the

necessary procedures to preclude running LPCI and/or Core Spray pumps

and testing ADS logic simultaneously. This LER is closed.

(Closed) LER 237/93011. Revision 00 and 01: Emergency Source of Water to

Containment Cooling Service Water (CCSW) Keep Fill Valved Out.

The

licensee added additional piping from the unit emergency diesel

generators to the respective CCSW systems during the spring of 1993.

This LER is closed .

18

. . .

r

{Closed) LER 237/93021: Defective Check Valves Due to Improper Bonding

of the Viton Seat.

The licensee determined the viton seat adhesive was

applied improperly.

The licensee completed an operability evaluation

and implemented contingency actions until the valves are replaced.

a

10 CFR 21 report was submitted on October 22, 1993.

This LER is closed.

{Closed) LER 249/91013: 250 Vdc Battery Discharge Voltage Decreased

Below Design Basis Limit Due to Inaccurate Vendor Data.

A Part 21

notification concerning the deviation was made in accordance with the

requirement of 10 CFR, Part 21, Sections 21.1.(B), 21.3.a(3), and

21.3.b(4). This LER is closed.

(Closed) LER 249/92012. Revisions 00. 01 and LER 249/92015, Revisions

00, 01, 02, and 03: Low Pressure Coolant Injection (LPCI) Minimum Flaw*

Valve Automatic Closure During Valve Operability Test. Certain volumes

of LPCI piping were de-pressurized during valve manipulation.

When

these volumes were re-pressurized, an instantaneous high flow was sensed

by the flow transmitter resulting in the closure of the LPCI minimum

flow valve.

The licensee revised Dresden Operating Surveillance (DOP)

1500-1, 1600-3, and 1600-5 to caution operation personnel. This LER is

closed.

(Closed) LER 249/93007: Reactor Scram on Reactor High Pressure, Possible

High Pressure Turbine Damage.

This LER is closed.

(Closed) LER 249/93014: Reactor Scram Due to Main Condenser Low Vacuum.

DOP 4400-8, "Circulating Water Flow Reversal," was revised which

established a minimum condenser vacuum on the low hood of 26 inches of

mercury and 27 inches of mercury on the high hood.

Additionally, a

caution was added to warn the operators that reversing condenser flow a

second time when no equipment problems are present should not be

attempted.

This LER is closed.

No violations or deviations were identified.

10.

Management Meetings (30703)

SALP 12 Meeting

On October 19, a public meeting was held in the Training Center at the

Dresden Station to discuss the Systematic Assessment of Licensee

Performance (SALP) 12 report for the Dresden Station. The list of

attendees is included in Attachment A.

Mr. John B. Martin presented

each section and encouraged discussion with the Commonwealth Edison

staff. Mr. Martin concluded the meeting by challenging management to

continue efforts to improve plant material condition, further develop

partnership between management and union personnel, focus on the 1994

goals, develop teamwork between departments, and improve leadership

behaviors .

19

The licensee provided a response to the SALP 12 report dated

November 10.

The NRC will continue to discuss planned improvements at

future management meetings.

No violations or deviations were identified.

11.

Inspector Followup Items

Inspector followup items are matters which have been discussed with the

licensee which will be reviewed further by the inspector and which

involve some action on the part of the NRC or licensee or both.

Inspector followup item disclosed during this inspection is discussed in

paragraph 3.b.

12.

Unresolved Items

13.

Unresolved items are matters about which more information is required in

order to ascertain whether they are acceptable items, items of

noncompliance or deviations.

Two unresolved items disclosed during this

inspection are discussed in paragraphs 3.e and 4.a.

Exit Interview (30703)

The inspectors met with licensee representatives (denoted in

paragraph 1) throughout the inspection period and at the conclusion of

the inspection on November 29, 1993, to summarize the scope and findings

of the inspection activities. The licensee acknowledged the inspectors'

comments.

The inspectors also discussed the likely informational

content of the inspection report with regard to documents or processes

reviewed by the inspectors during the inspection.

The licensee did not

identify any such documents or processes as proprietary.

Attachment:

Dresden SALP Meeting Attendees

20

Attachment A

OCTOBER 19. 1993 DRESDEN STATION SALP MEETING ATTENDEES

NRC ATTENDEES

J. Martin, Regional Administrator, Region III

W. Axelson, Director, Division of Radiation Safety and Safeguards

D. Chyu, Reactor Engineer, DRP

.

P. Hiland, Chief, Reactor Projects Section lB, Riil

C. Holden, SALP Program Manager, NRR

M. Kunowski, Senior Radiation Specialist

M. Leach, Senior Resident Inspector, Dresden

T. Martin, Deputy Director, Division of Reactor Projects, RIII

M. Peck, Resident Inspector, Dresden

J. Stang, Project Manager, NRR

A. Stone, Resident Inspector, Dresden

J. Zwolinski, Assistant Director for Region III, NRR

ILLINOIS DEPARTMENT OF NUCLEAR SAFETY

R. Schultz, Section Chief

C. Settles, Resident Engineer Trainee

R. Zuffa, Dresden Resident Engineer, IDNS

LICENSEE ATTENDEES

C. Reed, Senior Vice President of Energy Facilities

M. Wallace, Vice President and Chief Nuclear Officer

A. D'Antonio. Site Quality Verification Supervisor

L. Del George, Vice President, Nuclear Operations Support.

R. Flahive, Technical Services Superintendent

L. Jordan, Health Physics Supervisor

J. Kotowski, Operations Manager

M. Lyster, Site Vice President

H. Massin, Site Engineering and Construction Manager

T. O'Connor, Maintenance Superintendent

R. Radtke, Director, Support Services

R. Robey, Director, Site Quality Verification

J. Shields, Regulatory Assurance Supervisor

G. Spedl, Manager, Dresden Station

MEMBER OF THE PUBLIC

D. Kaufman, Chairman, Grundy County Board