ML17177A392

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Insp Repts 50-237/92-05 & 50-249/92-05 on 920303-0410. Violations Noted.Major Areas Inspected:Licensee Action on Previously Identified Items,Operational Safety & Preparation for Startup from Refueling
ML17177A392
Person / Time
Site: Dresden  
Issue date: 05/06/1992
From: Hsia A
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION III)
To:
Shared Package
ML17177A390 List:
References
50-237-92-05, 50-237-92-5, 50-249-92-05, 50-249-92-5, NUDOCS 9205150075
Download: ML17177A392 (23)


See also: IR 05000237/1992005

Text

'.'

U; S; N.UCLEAR REGULATORY COMMISSION

REG ION I II

Report No~.

50~237/92005(DRP); 50-249/9?005(DR~)

Docket No.s.

50-237; 50-249.

License Nos.

DPR-19;

DPR~2S

Licensee;

Commonweal.th Edison Company

Fac~lityName:. Dresden Nuclear PQwer St~tion, Units 2 and 3

Inspection At:

Dresden Site, .Morris, IL

Inspection Conducted~ March 3 through April

l~, 1992

.. Inspectors:* * . *

W. Rogel'.'S

M.

Peck

K. Shembarger *

D. Liao

A. Madi son

R. Zuffa; Site Resident Engineer

.

Illinois Department of Nuclear Safety" *

Ap-proved .'Bi:

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'

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  • " ;

.

l.>"'::Z.,. ;/jj 1-:=:f ' , i ' '/,; .* 2- ---

A. H. Hsia/ Actihg Chief .

Project~ Secti6n 18

Inspection Summary

1,' ) /. -. '

c

"' 6 / 'i L. '

I

.

  • Date *

Inspection from March 3 through Apr'il fQ,. 1992. (Report Nos. 50:-237 /92005CORP) ;"

.50-249/92005CDRP)).

. .

.*

....

Areas I~spected: .A routine unanno~nced safety inspection was conducted by the

resident inspectorsj and an Illinois Department of Nuclea~ Safety.ins~~ttor .

. lhe inspection reviewed licens~e action on previously ide~tified'.i~ems;

.

bpe~ational safety ind preparation for start up from refueling: Walk do~ns Of

. safety systems were performed and monthly maintenance. and surveillance

'-activities were *fol lowed~ Training effectiveness was evaluated, *as was

.

licensee handlirig of events. The licensee's saf~ty assessment and quality

. veiificati-0n capability was assessed and s~~eral ~anagemeht meetings were

held.

Re~ults: One vibl~tion with multiple*exa~ples of inadequate procedures or

inadequate implementatlon of procedures \\.{as i'1entified. Five unresolved

items~ -0he with multi~le examples~ and one open item was

identified~*

Plant Operations Control room operators were professional.

They were

.

knowledge~ble of annunciator alarms .. Reactor oper~tor log quality continues

to imp-rove .. Some fostances of-'inattentiori were-noted-~outside the control room

and some Technical Spec ifi cation kn owl edge defi ci enci es w_ere *noted.

Operator

identification and resolution of housekeeping deficiencies were not evident

except in the Unit 3 drywell where it was good.

Weaknesse~ were observ~d in

9205150075 920506

PDR

ADOCK 05000237

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.

PDR

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,

.

operator knowledge of administrative controls.*

  • Maintenance/Surveillance Maintenance activities appeared to be well performed

except for coordination.and completion of wcirk on the 2/3 di~sel fire pump.

Surveil 1 ance procedure content was a weakness .as was . imp 1 ementat ion of

surveillanc* procedures.

Emergencv Preparedness

Proper activation of the emergency plan was observed.

Safety Assessment and Quality Verification

There was limited mid-level

management presence in the power block. Safety evaluations for temporary

alterations were viewed as a weakness.

Engineering and Technical Support *Significant weaknesses in design basis

information and personnel's grasp of the information were evident.

The

  • weaknesses in the design basis information hampered operational dechions and

cost many hours of the licensee staff's time.

-

2

DETAILS

1..

Persons Contacted

Commonwealth Edison C6mpany *

  • C. Schroeder, Station.Manager
  • L. Gerner~ Technical Superintend~nt
  • J. Kotowski, Production Superintendent

D. Van Pelt~ Assistant Superintendent - Miintenance

J. Achterberg, Assist ant Superintendent - *Work Ptanni ng .

G. Smith, Assi.stant Superintendent-Operations

  • R. Radtke, Regulatory Assurance Supervisor

M. Korchynsky, Operating Engineer

1. Mohr, Operati~g Engineer *

  • M. Strait, Techhical Staff Supervisor
  • D. Ambler, Radiatioh* Protection Manager
  • K. Kociuba, Quality Assurance Superintendent
  • D. Karjala, Performance Improvement Director
  • Denotes.those attending-the exit inter~iew conducted on April 10, 1992:

The inspectors also talked with and intervi~wed several other licensee

employees, including ~embers of the te~hnical and engineering staff;

  • reactor and auxiliary operators; shift engineers .and .foremen;

elettrical, mechanical, and instrument maintenance petsonnel; and.**

  • contr~ct security personnel~
  • 2.

. Previously Identified Insp~ction Items {92701. and 92702)

a.

(Closed) Violations (50/237/90023-0la and b(DRP))~ Lack of*

. operations personnel knowledge of Dresden Administrative Procedure

.

(OAP) 7-5, Rev. 8, and Dresden Operating Abnormal (DOA) Procedure ..

902-S G-2, Rev. 3, and lack of technical staff personnel knowledge

regarding recognizing and processing conditions adverse to

qua l it,Y ._

Although this violation i~ considered closed, the corrective

actions to it appeared to have been inadequately implemented

resulting in repetition of similar events, as described iri

sections 2c(l) and 7c(l). The cause for the inadequate corrective

actions is under further review, and is being tracked as an

Unresolved Item (237/92005~0l(DRP)).

b.

(Open) Unresolved Item (50-237/91016-04(DRS)):

Em~rgenty diesel

generators (EDGs) breaker logic design cbnsisterit with existing

regulations.

The ltcensee routinely tests the EDGs loaded and

paralleled to the grid which renders the load shedding feature

nonfunctional. Should a loss of coolant accident coincident with

a loss of offsite power occur during t~e testing,_ rior!ll.aL " .

.

protective features*-would autonratfrallY be -bypas.sed, and the EOG

3

would be overloaded.

Under a*technical assistance request the

Office of Nuclear Reactor Regulation (NRR) reviewed this

situation.

NRR verbally provided the licensee and the inspe*ctors

  • with the following.initial conclusions: 1) An EOG is not capable

. of performing its intended function when .being tested in the

licensee's normal manner;

2) The .Technical Specification

requirement t~ demonstrate operabiliti of other EDGs when an IOG

is inoperable can be accomplished without performing a full load

  • test.

This matter rema-ins open pending written confirmation of the NRC

position, re~ponse from the licensee as to their position, and NRC

review of that response.

c.

(Closed) Unresolved Item (237/92002-04(DRP)):

Inoperable

containment isolation valve during VOTES testing~ While

performing VOTES testing on dayshift for Unit.3 isolation

~ondenser valve 1301-1 the operator de-en~rgized open the

isolation condenser valve 1301-1 on Unit 2, rendering it -

inoperable as a containment isolation valve.

Unit 2 was

operating at the time with containment integrity required.

An

oncoming swing shift senior licensed operator identified the

situation and power was immediately restored to the.valve.

.

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.

.

.

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.

During the-review of the situation the in~pector ascertained:

(1)

(2)

(_3)

Operators were _not cognizant of the administrative controls

associated with routine test activities as -discussed* in .

. OAP 7-32 "Routine Plant Testin~ Activities~. This lack of

knowledge of administrative. controls will be reviewed as

another e~ample of unresolved it~m (237/92005-0l(ORP)), *

inadequate corrective action to violatio~ 237/90023-01. *

.

.

.

.

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Locks were placed on the electrical breakers although np

equipment control program specified or directed their

installation. Plant staff occasionally placed locks on

electrical equipment for personnel protection;* These locks

are not part of th* equipment out-bf-service system, and are

not acknowledged to exi s.t by management. * No procedure

exists to direct the placement and use of the locks. This

is contrary to the requirements of 10 CFR Part50, Appendix

B, Criterion V and is considered one example of a violation

against that criterion (237/92005-02a(DRP)).

OAP 7-32 did not require specific measures to identify the

valve in test.

10 CFR Part 50, Appendix B, Criterion XIV,

  • inspection, Test, and Operating Status," requires in part

that measures be ~stablfshed to indicate the status ~f

testing performed upon individual items of the nuclear power

plant ... This is an example of a violation (237/92005-

02b(DRP)) of 10 CFR Part 50, Appendix B, Criterion V,

"Instructions, -Procedure*s, *and- Drawings," *in that the

4

procedure did not ade~uately prescrib~ activities affecting

quality .. Also, the applicable section of the CECo Quality *

Assur*nce*Manual doe~ not discus~ the application of OAP

7-32 for test control.

Two examples of a violation were identified in this area. Additionally, .

one unresolved item wtth .two examples was discussed,

3.

Operational Safety Verifi~ation (71707 & 717ldl

.

.

.

The inspectors reviewed the facility for conformance with the license

  • and with regulatory requirements.
  • a.

On a sampling basis the inspectors observed control room

activities* for proper control room staffing and c*oordination of

plant activities.

Operato~ adherence to procedures or Techni~al

Specifications and operator cognizance of plant param*eters and.

alarms was observed.

Electrical ~ower configuration was

.

confirmed and the frequency of plant and control room.visits by

station managers was reviewed.

Various logs and surveillance~

records were reviewed for accuracy and completeness .

. The inspectors noted that the quality of control room operator log

entries tontinued to improve.

The logs were generally ~dequate as

to the content of the entries.

b.

On a routine basi~ the inspectors t9ured accessible areas of the

facility to assess worker adherence to radiation controls and the

.site security.plan, hoOsekeeping or cleanliness, and control of

field activities in progress.

Significant observations were:

The ~~it 3 drywell was exceptionally .clean prior to and at

the time of the drywell close out inspection.*

. '

-Housekeeping in the Unit 2/3 crib house, auxiliary

electrical room. and the 4160 VAC ESF Bus 23 and 24 room was

poor.

Following maintenanc~ of the 2/j diesel fire pump, trash was

left in the area, oil was spilled on the floor, and several

drop lights were strung about.

c.

Walkdowns of *select engineered safety feature~ (ESF) were

performed.

The ESFs were reviewed for proper .valve* and electrical

ali~nments. Components were inspected for leakage, lubrication,

abnormal corrosion, ventilation and cooling water ~upply

availability. Tagouts and jumper records wer~ reviewed for

accuracy where appropriate.

The ESFs reviewed were:

5

Unit 2

Unit 2/3 Standby Gas Treatment System

. *

  • Unit 2/3 Diesel Generator

Unit 3

All Main Steam Isolation Valves

Unit 3 Diesel Generator

No violations or deviations ~ere identified in this area.

4.

Preparation for Start Up from Refuel i nq

In preparation for Unit 3 startup *from a scheduled refueling ~utag~, the

inspectors performed a number of administrative control ~dequacy reviews

and physical walkdowns of safety systems for material condition

discrep~ncies and proper valve, switch, and electfic~l alignments.

a.

Admini~ir~tive ~ontrols reviewed were the out-of-servic~ (OOS)

equipment controls, high radiation door access, temporary

alteration implementation, locked cabinets containing necessary

tools for implementation of the emergency dperating or safe

.

  • shutdo~n procedures (EOP/SS) and the su~veillance tracking system .

. * Reslil ts were:

  • (1) * Out-of-service (OOS) - The program was acceptable.

However,

some OOS tags had been in place for* an excessive period of

.time.

An example was the OOS tag on MOV 2/3-4101, fire pump

discharge valve.

This valve h~d been out~of-service for

approximately 12 ye~rs following the Three Mile Island

(2)

  • Action Pl an.

Another example was the OOS tag on the St'andby

Gas.Treatment damper, 7503.

This damper had been

deenergized to preclude a single failure concern.

Use of

..

the out-of-service system as a de facto minor modification

    • is considered a weakness in the program .arid i~ an open item.*

(237/92005-03(DRP)) to.follow licensee corrective actions.

High Radiation Door Access - All high radiation doors were.

locked; Two-locations of minor concern were identified:

(1) The fuel pool ~ooling (FPC) area, a high radiation area,

could be reached from the fourth floor via a ladder.* _Access

to the ladder was restricted by a cage which surrounded

. part of the ladder; 'however the cage "was not 1 ong enough to

prevent personnel from using the ladder.

(2)

A fence on

the turbine shield wall west side did nbt have a Tock.

Othef similar fences were secured with chains and locks.

These inspection findings were brought to the licensee's

.*attention. Preliminary corrective actions were in progress .

. (3)

Temporary Alterations (T/A) -

Five T/As were targeted to be

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(4)

(5)

in place for startup. One dealt with installation of

diagnostic equipment on the isolation condenser.

When the

instrumentation was installed, personnel failed to update*

  • critical drawing, M-359, wit~in a day of installation as

. required by the T/A procedure, DAP-07-04, *control of

Temporary System Alteratio*n,* step F.l.f(S) .. Failure to

acc6mplish this task as prescribed in the procedure is

considered another example of a 10 CFR Part so, Appendix 8,

Criterion V violation (237/92005-02c(DRP)) *

. EOP/SS Cabinets - All. equipment necessary to perform the

. EOP/SS functions was present in the audited cabin~ts.

Surveillance Tracking System ~ No discrepancies or overdue

surveillances were identified.

b.

  • System walkdowns were performed on the following systems:
    • * **
  • *
  • * *

Low Pr~ssure Coolant lnje~tion System

Standby Liquid Control System (SBLC)

Core Spray System

Standby Gas Treatment System* (SGTS) .

One bank of Hydraulic Control Units

.containment Cooling Service Water (CCSW) System

Emergency Diesel Generator Cooling Water System

.

Emergency Diesel .Generator Air Start System (Unit 3 .and ,2/3)

.Fire Protection System

Significant observations were:

(1)

On April 1, 1992, the SBLC storage tank air sp~rge in)et

valve 3-1101-36, was found open and unlocked .. The system

valve lineup checklist ;n*oop 0040-M4 required the valve to

  • be locked closed and independently verified in that *

position~

The valve was manipulated *on March 20, 1992, to facilitate a

SBLC storage t~nk.air sparging prior to sodium pentaborate

sampling.

OAP 7-14, ~Control and Criteria for Locked

Equipment and Valves", required eit~er an approved procedure

or outage checklist be used to unlock lnd reposition a

locked valve. If a valve was unlocked without a

corresponding procedure' or outage checklist, an operator *was

required to be in continuous attendance~ Final valve

  • position was required to be in accordance with the equipment

checklist, independently verified by two individuals, and*

documented in the unit log book.

The. ai-r sparging * ev.olution

was performed without an approved procedure or outage

checklist. Additionally, the locked v~lve was repositioned

without an operato*r in continuous attendance. This

7

personnel failure to understand and execute administrative

requirements is another example of the unresolved item

mentioned in section 2.a (249/92005-0l(DRP)).

(2)

On April* 1, 1992, a wal.kdown of the Unit 2 and Unit 3 SBLC

. * systems was performed.

DOP 0040-M4 required .the f o 11 owing

  • valve~ to*be locked in the correct position~

(3)

(4)

(5)

. *

2A-1150, pressure indic~ting root valve

  • *

3A-1150, SBLC pump discharge root valve

30..:1150, SBLC pump discharge indicating backfill valve.

The valves were in the correct position with a locked chain ,

draped over the operator. However, the chain did not

restrict operator movement.

OAP 7-27 *independent

.

Verific~tions" states:

"Th~ last.per~on to check a lricked *

valve will also ensure the locking devi~e is installed .

  • properly (i.e. the ch~in will not fall off}.

I~ is not the

intent of a locking ~evice to pr~vent movement of a valve

but to serve as a flag to indicate that before this valve is*

manipulated certain precautions or actions may be required".

The practice of draping a lock and chain across a _valve

instead 6f physically securing to prevent movement is

conside*red a weakness in the.conduct of operations.

CCSW pumps A & D leaked.exces~ively thrbugh the packing and

. work request tags identifying the condition were present. ..

The most current ASME inservice tests Qn the pumps met *

required* ~ressures and flows with the A pump in the "Alert~

region.

At the end of the inspection peiiod, Technical

Staff persohnel were determining the priority of a m~nor

modification for installing new CCSW pump shafts.

A minor drawing discrepancy .was identified by the inspectors *

on the Piping and Instrumentation Oiagram (P&ID} for the

.

Standby Gas Treatment System dealingwith the location of a

  • lotal temperature indicator on each train. Once identified

to the 1 i censee, a P&ID change request was submitted.

Several di~trepancies ~ere noted between the a~tual fire

protection system and the associated P&ID.

Also

  • discrepancies were noted between Dresden Fire Protection

Procedure (DFPP} 4120-Ml, the system's proper alignment -

checklist,- and equipment nameplates.

The discrepancies were

due to a modification to the fir~ protection system to

support the new ~dministrative and service building *

additions.

The fire protection system loop modification was completed

during November/December 1991.

Retagging of the ~qujpme~t

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was in progress. The licensee had walked down the*fire

protection system during February and March 1992 and

submitted a P&ID change request.

The discrepancies were

  • discussed with the licensee and the correct system lineup

was verified by the inspector and Assistant Fire Marshall.

After the P&ID is changed, the DFPP will be revised and

updated to reflect the modifications.

O~e example of a violation was identified in this area.

One exa~pje of

a previously mentioned unresolved item and one open item are 'discussed

in this section.

5.

Engineered.Safety Feature System Walkdown C71710)

A detailed walkdown of the accessible portions of the Unit 3 Isolation

Condenser System was performed to verify systeni operability. The

lso.lation Condenser i.s relied upon.during implementation of the Dresden*

Emergency Operating Procedures (DEOPs), and is the primary method.of

. *decay heat remo.va 1 in the Dresden Safe Shutdown Procedures (DSSPs).

a..

While reviewing documentation associated with the 'makeup water.

supplies to the isolation condenser, the inspector identified

several issues and discussed them with the licensee. These issues

  • .. are unresolved (237/92005~04(DRP)) pending ftirther licensee

evaluation of these concerns and additional NRC review.

.

.

lhe*original fire suppression system hydraulic verification

study performed for the Dresden Station ~ay not have been

based on the most bounding condition.

  • *

The DSSPs do not direct operators to .open the crosstie valve

between the IA condensate storage tank (CST) and the 2/3 CST

although the lA.tST water volume is used t6 ensure minimum

safe shutdown water volume availability.

.

.

Discrepancies appear to exist between DSSPs, the Safety

. Evaluation Report (SER) and the Fire Hazard Analysi~ as to

th~ intended isolation condenser makeup sources.

Discrepancies in the hydraulic verification study and the

DSSP requirements for use of water sources challenge the

ability of the Fire Protection System to support both makeup

to the isolation condensers and*suppress a fire.

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Attachments to DSSP 100-CR "Control.Room Evacuation/ Safe

Shutdo~n" did not contain some.local operator actions tha~

were specified in the body of the proced.ure.

Additional confirmation of the actual CST useable water

volume was necessary, including confirmation of the accuracy

of the level instrumentation and its presence._i~- a

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  • ,,

.,

calibration program.

When DSSPs were .revised in April, 1988, the 10 CFR 50.59

~afety evaluations failed to consider the ~ostulated 10 CFR

Part 50, Appendix R, fire scenarios. as part of the facility

design basi~.

b.

During a physical walkdown of the isolation condenser system,

valves 3-1301-32 and 3-1301-19 were found to be ciosed as

required, but the chains and locks associated with the valves

allowed the valves to be opened without removing the locks. Thi~

finding" was consistent with those presented in sectjon 4.b.2.

After identification.to station personnel, both valves were

adequately locked.

c.

Minor drawing discrepancies*were identified and brought to the

attention of station personnel for resolution including:

Hanger # M-1199D-262 on drawing ISI-206 appeared to be"""'

reversed with its. adjacent snubber ..

Valve 3-1301-10 was identified as being powered from

emergency AC power instead of DC power on drawing M-359.

The primary makeup supply (clean demjneralized water)

connection to the isolation condenser system ~as not

identified on drawing M-359.

  • *

d.

bop J300~M1/El "Unit 3 Isolaiion Condenser~ step 39 required valve

  • 3-1301~603 to be closed and step 50 required valve 3-4107-50~ to

be open. During performance of the DOP on February 24, 1992, the

checklist performer and idehtifier indicated on the checklist that

the valves were actually locked in their designated positions.

No

documentation to correct the ~hecklist was identified.

The

inspector verifi_ed that both valves were locked in the identifi.ed

positions. These dis~repancies were i~entified to station.

personnel for review and ~esolution.

No violations Or deviations were identified.

One ~nresolved item was

discussed.

6.

Monthly Maintenance Observation (62703~ *

=St~tion maintenance activities affecting the safety-felated arid

  • important to safety systems and components listed below were observed

and-reviewed to ascertain th~t they were conducted in accordance with

approved procedures, regulatory guides and industry codes or standards,

and did not cOnfl ict with Techn*ical Specifications.

The following item~ were considered during this review: . ~pprovals were

  • obtained prior to initiating the work; functional testing or

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  • * *

.

.

calibrations were performed prior to returning components or systems to

service; quality control records were maintained; activities were

accomplished by qualified personnel; parts and materials used were

properly certified; radiological controls were implemented; and fire

prevention controls were implemented. . *

  • The following maintenance activities were observed and reviewed:

Unit 2

Unit 2/38 Standby Gas Treatment charcoal * filter replacement &

repairs

..

Unit 2/3 Diesel Generator rotor p9le bolt re-torque/replacement

Unit 2/3 Diesel Fire Pump repair

lJnH 3

  • * **
  • *
    • * *
    • ** * * *

Traversing incore.probe amplifier power supply*repair

Control rod drives P-7 and E-3 replacement

High Pressure Coolant Injection (HPCI) full flow test throttle

valve, 2301-10, replacement

  • Core Spray injection valve, 1402-248,'repacking
  • 8 Feedwater line containment penetr.ation (X-1078) replacement

Main Steam line penetration (X-1058) bellows repair

.. ,

Emergency Diesel Generator rotor pole bolt re-torque/replacement

West bank scram discharge volume vent isolation valve rebuild .

Reactor building v~ntilation damper air lines seismic support .

installation .

.

  • .Stator cooling panel modificati~n

.

Safety relief valves acoustic ~onitor installation

HPCI turning gear motor limit adjustments

.

  • EHC and Main Stop.valve pre-operational line up work

.

.

.

Inboard and outboard Main Steam Isolation Valves (MSIV) pilots and *

cylinder operator replacement or repair.*

Electrical penetration (X-202S) repair

Annunciator fuse block replacement

Significant ob~ervations were:

a.

The inspector observed. overall good convnunications between working

individuals with an improved attitude toward procedure usage and

b.

work package guidelines.

During MSIV maintenance activities on March 17, 1992, the

inspector observed *a missing pilot valve terminal junction box .

supporting bracket on the 3~2038 MSIV.

The inspector located the

bracket lying on the structural support ste~l directly above the

valve.

The support bracket's function appears to prevent the

terminal box from pivoting and inducing moment forces .at the pilot

solenoid connection.

The inspector determined from a review of

the valve maintenance history that the latest maintenance acti~i!.Y ..

11

. *-

on the valve operator assembly was perfonned on February 10, 1990.

The support bracket for the other MSIVs was intact. *This matter

is.unresolved (249/92002-0S(DRP)) pending further inspector review

_as to whether the support bracket was essential to the integrity

of the MSIV valve operator.

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c.

At 1534 on February 28, 1992, the 2/3 Diesel.Ffre Pump *was taken .

out of service for gasket replacement to repair an oil leak.

Removing the 2/3 diesel fire pump from service resulted in entry

into Dresden Administrative Technical Requirement (DATR) limiting

Condition for Operation (LCO) action statement 3.1.2.1.a, which

required the fire pump be rest-0red to _operable status within 7*

days or a deviation report prepared.

On March 6, 1992, at 2030,.

the 2/3 Diesel fire Pump was returned to service, and a deviation

. report was prepared s i nee the *se.ven-day LCO was exceeded. The

deviati.on report did a time study analysis *of the event. *

The inspectors and the licensee agreed on the following sequence

of events:

The diesel fire pump was removed from service two shifts*

priQr to the_start of maintenance activities .. *

Maintenance activities were halted for five shifts due to *

  • management request.

.

.

The original replacement gaskets to stop the oil leak.were

th_e wrong material. The work analyst had improperly

classified the gaskets as non-safety related instead of

regulatory re 1 ated. * Therefore, receipt inspection was

minimal and didn't identify the material discrepancy.

It took two *days for the purchase order for the right .

  • gaskets to be prepared and issued to the vendor .

Th~ parts were delivered to ~he station two shifts prior t6

di scoverY that they were on s*i te.

Due to a part number discrepancy, there was a one hour delay

during the receipt ~nspection.

The licensee attributed the root cause of exceeding the_L~O to an

expansion of work scope during the fire pump repair. The

inspectors, on the other hand, attributed the root ca~se to the *

six delays discussed above;

The licensee's corrective action was

to discuss the event with personnel to heighten their*awareness. *

The inspectors considered these corrective actions minimal.

d.

While witnessing annunciator troubleshooting and ~ubsequent fuse

block replacement, inspectors observed:

12

A fine layer of dust was on all the control annunciator

circuit boards.

  • An operating standard .commercial drinking fountain was** *

located in the auxiliary electriC:al equipment.room,.which

contains numerous safety related equipment.

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.

Extremely large gauge wire was used for the negativ~ circuit

which may have contiibuted to the loss of ~ll control room

annunciators on Alert of April 4, 1992.

.

. ..

In response to these observations, the licensee vacuumed the

cabinets and was trying to determine whether a periodic

preventative maintenance cleaning was appropriate and, unplugged

.the drinking fountain and tagged it out of service. With regard

to the large gauge wire .the licensee stated they kne~ this and an

  • annunciator circuit modification was being contemplated.

No violations or d~viations were identified.

One Unresolved item was .

discussed.

7.

Monthly Su~v~illance Obs~rvation (617~6)

Surveillance testing required by Technical Specifications, the Safety*

Analysis Report, maintenance activities or modification activities w.ere

observed or reviewed.

Areas of consi-deration while performing

.

obsefvations were procedure adherence, calibration.of test equtpment,

identification of test deficiencies, and personnel qualification. Areai *

of considerati6n while reviewing surveillance records were completeness,

pro~er a~thorization and review signatu~es, test results properly*

. dispositioned, and independent verification documented~ *The following

activities were obser~ed or ~eviewed~

Unit

    • *

Unit

    • * * * * * * * *

2

3

DIS. ~00-2

Control Rod Dri.ve Accumulator Pressure Switch *

Calibration

DIP 700-ll Calibration of the TIP.

DIS 2301-:-03 HPCI High Flow Isolation Calibration

DTS-1600-01 LLRT of Primary Containment Isolation Valves

DTS 1600-04 Local Leak Rate Testing of Elettrical Penetraticins

DTS 7500-07 Standby Gas Treatment System Charcoal Leak test

DTS 7500-11 DOP Testing of 2/3 *SBGT HEPA Filters

1400~01 Core Spray System Pump Test *

DOS 1400-02 Core S~ray System Val~e Operability Check

DOS 1400-05 Quarterly Core Spray System Pump Test

DO~ 1500-06 LPCI System Valve Operabil1ty Ch~ck

DOS 1500-02 .Containment Cooling Service Water Pump Test

13

.

. ' :*

DOS 1500-10 Quarterly LPCI System Pump Test

DOS 6600~03 Bus Undervoltage and ECCS Integrated .Functional Test

for Unit 2/3 Diesel Generator

DOS 6600-04 Bus Undervoltage and ECCS Integrated Functional Test

for Unit 3 Diesel Generator .

  • SP 92-3-57 Bus Undervoltage*and ECCS Integrated Functional Test

for Unit 2/3 Diesel Generator

.

DIS. 600-2

Narrow Range Reactor Pressure Calibration

DIS 600-3

Reactor-Vessel Narro~ Range Level _

.

DIS 1400-06 Core Spray Flow Transmitter FT 1461A(B) Calibration

and Maintenance Inspection

DIS 1400-07 Core Spray Pump Minimum Flow Valve Analog Trip Unit

Calibration

DIS 1400-01 Core Spray Header Differential Pressure

Instrumentation Calibration

DIS 1500-19.LPCI System Pressure Transmitters and IST Pump Suction

  • Discharge .Pressure Indicators. Ca 1 i brat ion
  • .

DMP ll00-1 * Standby Liquid Control Squib Valve Inspection

Sighificant observations ~~re:*

a.

Drywell Air Sample

On March 8, 199~, station personnel did ~ot complete the Unit 2

Reactor Coolant System (RCS) leakage T/S Surveillance (4.6.d)

within its normal time interv~l. The previous s~rveillance was

  • completed at 11:45 A.H. on Ma~ch 7, 1992.

The next surveillance

was not completed until 4:13 A.H. on March 9, 1992 .

. Technical Specifi~atio~ surveillance requirement 4.6.d delineates

t_hat. a drywell air sample will be taken daily and analyzed to

determine whether the reactor coolant leakage is within acceptable*

limits.

  • 9:20 a.m. on the 8th, the health physics (HP) technician retrieved

the* drywell air samples from the continuous air monitor (CAM) and *

determin*ed the sample was invalid since .the CAM was not runnin*g~ *

A second sample .was taken from an alternate. sample point and ..

delivered to Chemistry Department.

At 2:51 .P.H. the chemist

completed the sample count but failed to communicate the results

  • to the control room.

At 11:00 P.M. the d~parting SCRE reviewed .

and initialed Appendix A, Unit Operator~ Daily Surveillance Log,

indicating that all of the shift operational ~urveillan~es were

successfully completed.

However, the block for T/S 4.6.d was left

blank.

The SCRE and the reactor operator recognized the drywe11*

. air sample results were not completed.

However, they failed t~

recqgnize the sample analysis was required to meet the RCS .leakage

surveillance. The operations personnel incorrectly beli~ved the

samples were only needed for the drywell venting procedure .. At

4:13 A.H. on March 9th the reactor operator decided to vent the

~ . *- -

.. :: -

14

Unit 2 drywell .. This decision prompted the Chemistry* Department

to ~ommunicate the sampl~ results to the reactor operator.and the

appropriate log entries were made.

The midnight operations crew

also failed to recognize the sample analysis was required to meet

the RCS leakage T /S requirement.

From this chronology*and a*review of the surveillance procedure

the inspector determined:

(1)

(2)

The RCS l~akage surveillance procedure; part of the Unit

Oper~tors Daily Survei.llance Log (Appendix A), nomenclat4re

was inconsistent with T/S 4.6.d.

The procedure step was

labeled"Drywell CAM Filter Readings, 6-hour BETA GAMMA

Micro Ci/2cc from Chemistry Department".

This nomenclature

did not agree with the T/S requirement, "Reactor coolant

system leakage shall be checked daily by the sump and a.ir

sampling system

11

Appendix A required the reactor operator to record "N/A"

.following successful completion of the surveillance each

day.

Use of

11 N/A

11 was misleading indicating the requirement *

was not applicable.

(3)

The survei~lance procedure;~ acce~t~nce criteria shown in

the U~it Operators Daily Surveillance Log (Appendix A) was

based upon drywell venting not reactor coolant leakage. *

This is another example of an activity affecting quality not

being covered by a procedure, and.is another example of the

previous violation (237/92005-02d(DRP)) ..

( 4.)

(5)

(6)

The inspectors determin~d that several SEs and SCREs failed

to recognize that failure to meet T/S surveillance

requirements constituted a failure to meet the Limiting

Condition for Operation (LCO).

The.RCS Leakage T/S LCO

Action required ~n orderly shutdown to be initiated and the

reactor shall be in a cold shutdo~n condition within 24*

hours. *The operato'rs concluded the LCO action was not *.

applicable even when the surveillance requirements are:not

met (excluding the 25% surveillance interval ma*ximum

allowable ~~tension): This is considered a weakness in the*

conduct of shift operations.

The licensee's surveillance program is based on a daily

versus 24 hour2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> routine, however, the policy regarding

11Daily

11 has not been clearly stated.

The licensee indicated

such a policy would be written.

The HP technician's acti.on to resample upon discovery of the

  • inoperable CAM,- and the associated log entries,* indicated a

positive, questioning attitude.

b.

On March 11, 1992 the inspector observed the HR.Cl High Flow

15

Isolation Calibration per DIS 2301-03: After the HPCI steam

valves were i~olated, the LPCI minimum flow valve 2-1501-138

clo~ed automatically.

The analog trip unit (ATU) for the HPCI

high flow transmitter was located adjacent to the LPCI minimum

flow ATU.

The instrument mechanic indicated that he had selected

the correct ATU on the master calibration unit. * Through

subsequent discussions and a review of the~ircumstances, the

inspector concluded the wrong ATU was inadvertently selected on

the master calibration uni.t.

c.

On March 7, 1992, the licensee performed DOS 6600.:.03. * During a

record review of the completed procedure, the *fo 11 owing

observations were made:

(1)

During the test, the 2/3 Diesel Generator ~ent fan and fu~l

oil transfer pump fajled to transfer to Unit 3 power when

expected.

( 2) .

OAP 9-11, "Procedure Usage and Adhetence" Rev. 3, requires a

Procedural Comment Supplement, Form*9-11A, be completed if

unexpected responses occur.

The form is to be used to

document information such as the destription of the. problem, :

the basis for continuing or discontinuing the procedure, the

steps or prcicedures fcillowed to return the line-up to

normal, and .the names of p~rsonnel contacted as part of the

decision making pro~ess.

.

.

.

.

The licensee did not document the unexpe~ted responses to

the test fo the manner prescri b.ed by admi ni strati ve .

.

procedures (no Form 9~11A wa~ com~leted).

Also~ based upon

interviews, the test leader and a technical support staff

group leader involved in the test were riot aware of Form

9~11A or the procedural* requirement, and did not recall.

receiving training on OAP 9~11. This is another item to be

  • reviewed under Unresolved Item {237/92005-0l(DRP));

During the test, sever:a 1 steps were performed locally by

station pe~sonnel, under the dire~tion of the test leader in

the control room.

OAP 9-11 required initialing or signing of a step be based

on either direct observation, or a direct report (a.g.,

telephone call, face-to-face communication) from the person

  • making the observation.

It further states that if other

than direct observation is utilized, then the initials of

the person performing the observation must be included with

the initia*ls of the person actually initialing the step.

Severa 1 of the steps performed locally by station per.sonne 1

were signed with only the test leader's initials, although

direct observation of step p~rformance was not utilized .

The failure of key personnel ~o:~e ~ognizant of-applicable

16

administrative procedure will be a reviewed as another

example of unresolved item (237/92005-0l(DRP)) of 10 CFR 50

Appendix B, Criterion XVI, Corrective Action in. that the

corrective action to violation 237/90023-0l(DRP)*was not

adequate to preclude this situatiori~

(3) *

Two of the acceptance criteria for DOS 6600-03 are .

verification that the diesel generator operates with the

emergency 1 oads 1 oaded for greater than five minutes and for

the 2/3 di~sel generator auxiliary equipment feeds to

automatically transfer.to Unit 3.

The documehtation for loaded diesel generator operation was

inconclusive as to.whether the five minute requirement was

met.

Therefore~ process computer data was reviewed and

confirmed that the emergency loads had been unloaded from

the emergency bus prior to completion of the minimum five

minute run of the loaded diesel generator.

The failure to

run the EOG in a loaded condition for five minutes in

accordance"wi th step I. 7. a of Dos* 6600-03 is another example

of a 10 CFR Part 50, Appendix B, Criterion V, violation

(249/92005-02e(DRP)) for failure to follow established

proc.edures.

  • Also, the documentation was uncle~r as to whether the 2/3 *
  • diesel generator *auxiliary equipment automatic transfer to

Unit 3 w~s verified .. A butned cable prevented the

ventilation fan from transferring and an i~properly

installed relay cover inhibiting the movement of a relay

, prevented the fuel oil transfer pump from transferring.

It

was subsequently confirmed that, following replacement of

the burned cable and removal of the relay covet, the vent

faD and fuel oil. transfet pump were loc~lly st~rted fro~

Unit 3 power.

Therefore, automatic transfer of all 2/3

diesel generator auxiliary equipment was not verified d~ring

performance of the survei Hance procedur.e.

After bein~ informed that the acceptance criteria had not

been met, the licen~ee successfully performed Special.

Procedure (SP) 92-3-57, "Bus Undervoltage Arid ECCS

Integrated Functional Test For Unit 2/3 Diesel Generator

{Unit 3 Test Only)", on M~rch 21, 1992, and verified the

diesel generator operated for greater than five minutes

while it was loaded with the emer~ency loads and the 2/3

.diesel generator auxiliary equipment feeds transferred to

Unit 3 .. The inspector observed test performance and.

reviewed the completed test procedure and verified the

established acceptance criteria were satisfied.

A further_example of a violation was identified.

Two examples of ~n

unresol.ved item were discussed .

. 17

y

8.

Training Effectiveness {41400, 41701)

The effectiveness of training programs for licensed and non-11censed

personnel was reviewed by the inspectors during the witnessing of the

licensee~~ perform~nce of ro~tine ~urveillance,. m~intenance, and

  • . operati6nal activities, and during the review of the licensee's response

to events which occurred during the inspection period.

Plant personnel

exhibited. weaknesses in knowledge of the reactor coolant leakage

Technical Specification requirements and knowledge of administrative

procedures for testing.

No violations or deviations wer~ identified.

9.

Events Followup {93702*).

During the inspection p~riod, several events occurred, some of which

required prompt notific~tion of the NRC pursuant to 10 CFR 50.72.

The

inspectors pursued the events onsite with the licensee and with NRC

~fficials. In each case, the inspectors reviewed the accuracy and

tim~iness of the licensee notification, the licensee's corrective*

actions and that activities were conducted within regulatory

requirements.

The specific ~vents reviewed w~re:

a.

Ori April 2, 1992, the Unit 3 reactor operator started the 3C ~nd

  • 3D c6ntainm~nt cooling.service water (CCSW) pumps iTI parallel to

assist pump packing adjustments by maintenance personnel.* Th_e

reactor operator observed 5600 g~llons per minute (GPM) total

flow.

Subsequently, the reactor operatot started the JA and the

38 CCSW pumps in parall~l and observed 5300 gpm.

These flow rates

were tonsiderably less than the 7000 gpm specified in DOP 1500-2, *

"Torus Water Cooling Mode of Low Pressure Coolant Injection

. System," for such pump configurations.

The condition was reported

to shift management, appropriate log entries were made ~nd a**

significance condition adverse to quality report was

i~itiated.

Subsequent testing of-the Unit 2 pumps reveal~d 7000 gpm could not

be achieved for those applicable pump combinations.

C~rtain portions of design basis documents i~fer the *need for 7000

gpm CCSW flow to.maintain an acc~pt~ble torus water temperatur~.

These include Final Safety Analysis Report (FSAR) Table 6.2.4-1

"LPCI/Containmerit Cooling Equipment Specifications" and FSAR

Section 5.2.3.2 "Containment Response to a -Loss of Coolant

Accident." Another design basis documents, General Electric

drawing 729E583 "LPCI containment cooling system process flow

diagram", completed "in 1969, reflected 7000 gpm ccsw flow in a

particular operational mode.

Other sections of d~si~n bas~s_

documents indicate only 3500 gpm is needed which correlates to one

CCSW pump in operation to maintain acceptable torus water

temperature. The need of one CCSW pump is consistent with

emergency diesel generator electrical loading capacity.

Also, in 1988 the licensee completed a safety e.valuation-:and* *

18

modification package to replace the copper nickel LPCI heat

exchanger tubes with stainless steel. Tube replacement resulted

in ~n approximate 10% degradation in the overall heat transfer

coefficient for the heat exchanger.* Calculations supporting the

safety evaluation were based 6n a 2-LPCI pump 2-CCSW pump

capability.

Since Unit 2 was operating and Unit 3 was in cold shutdown, an

operability evaluation was conducted for Unit 2 and completed on

April 4, 1992.

This evaluation coricluded that the CCSW system ~as

c~pable of performing its*safety*function in a one CCSW pump (3500

gpm)/one LPCI pump configuration. A safety evaluation was

performed prior to restarting Unit 3 and reached the same

conclusion -for that unit.

This isiue is ccinsidered unresolved (2~7}9200~-06(DRP)) pending

further NRC evaluation of the li~ensee's HPCI heat exchanger duty**

and suppression pool temper~ture calculation to support operation

of both ~nits, the 10 CFR 50.59 safety evaluation for the 1988 .

heat exchanger tube change out, and th~ original General Electric

design* calculation to support the process flow diagram.

.

.

'

. .

b.

On April

2~ 1992, while Unit 2 was at 98% power, .the licensee.

identified the post-atcid~nt in~trumentation Technical

Specification surveillance requirement for daily source range

  • monitor instrument checks and quarterly calibration checks-may not:

ha~e been performed as required. The apparent ca~se was *

misinterpretation of the Technical Specifi~ation requir~ments.

This issue is considered.unresolved (237/92005-0?(DRP)) p_ending *

further evaluation PY the NRC.

c.

On~March 19, 1992, the licensee informed the NRC that a licens~d

operator tested positive for marijua.na iff a random fitness-for..:.

duty te~t. The individual was_ suspended for 14 days acco~ding t~

the.licensee's Fitness-For-Duty p~ogram and referred to the :

, Employee Assistance Program for assessment.

This matter h-as been

  • directed to the Operator Licensing section at the NRC Regional

office. -*

.

.

d. * * On April 4, 1992, with Unit-3 in ~old shutdown, the licensee

  • declared an Alert du~ to the loss of Unit 3 control room

annunciators.

The loss of the annunciators was. caused by a loose

wire on the negative side of one of the control room panels.

However, due to the design of circuits all th~ control room panel *

  • negative circuits were "daisy-chained" together. Therefore, by

losing continuity of one circuit, all the circuits failed.

The

licensee properly classified the event and manned appiopriate

command centers. The event was terminated with the restoration of*

the .anh~nciator system on April 5, 1992.

e;

On March 14, 1992, the high pressure coolant injection (HPCI)

suction valve (MOV 3-2301-6) unexpectedly opened duriri~ the Unit 3

19

.*

integrated .leak rate test {ILRT) .. The MOV opened during ILRT *

pressurization when the high drywell pressure setpoint was reached

providing an engineered safety features {ESF) actuation signal to

the HPCI system.

No othei valves or devices in the HPCI -system*

changed state.

Station personnel intended to remove the MOV from service.prior to

pressurization.

In prepatation for the llRT, el~ctricians were to

disable the actuation signals to all ESF equipment.

For the MOV

this was to be accompli~hed by lifting two wires in the MOV

control circuit. However, the electrician removed the wires from

the corresponding terminal block and taped them together

maintaining the ESF actuation circuit in service. *

.

.

Onshift operations management failed to recognize the opening of

. the MOV wa~ an unplanned ESF actuation and did not report the

event within four hours vi'a the emergency not ifi cation system

{ENS) per 10 CFR 50.72(b){2)(ii).

Following.NRC inspectof

. inquiries, th~ next day off-shift management reviewed the event

and determined a 10 CFR 50,72 report was appropriate.

The report

was made on March lB, 1992.

This is the- third time in less than eighteen months that the

licensee failed to make an ENS report due to an unplanned ESF

actuation .. Two previous violations associated with 10 CFR 50.72

were. issued for failure to make the required NRC notifications*

  • following ESF actuation on December 8, 1990 and July 4, 1991. ,

In response to the first violation the ~jc~n~ee issued a

memorandum to the operations personnel to provide guidance on the -

defi~ition of an ESF actuation.

Th~ gtiidance defined an ESF

actuation to include ~ny non-planned or unknown occurrence

invblving the actuation of an ESF train, which results in the *

completion of the desired re~positioning of any piece of

equipment.

Following the July 4, 1991, failure t~ report, the NRC issued a*

violation of 10 CFR 50, Appendix B, Criter~a XVI, Corrective

Actions, for the ineffective corrective actions from the previous

violation.

In response to the second.violation the licensee

committed to:

e

Provide training to the shift engineers (SE) and shift

contiol room engineers {SCRE)~

Clarify the guidance provided operations personnel.

The

clarified guidance defined an ESF actuation as:

"Unplanned

actuation of ESF systems ot compon~nts thereof {e.g.,_valve

movement, pump starts) are expected to be reported

tegardless of what caused the actuation, even if the

actuation was unnecessary or was not directly initiated by

20

  • .. *.-

..

ESF actuation signals."

Develop a flow chart to aid in ascerta.ining reportability

requirements and provide it by early first quarter, I992.

. Tp place a copy of NUREG I022, Licensee Event Reporting*

.System, in the control room to aid in reportability

determinations.

The reasons why the corrective actions to prevent recurrence of

the previous violations were not effective will be further

reviewed by the NRC.

This is considered another example of the

unresolved item di~cussed in section 2.a (237/g2005~0I(DRP)).

.

'

No violations or deviations were identified; however, twb new unresol~ed .

items and another example of a previously identified unresolved item was

discussed.

IO.

  • Safety Assessment and Quality Verifi~ation (40500)

ai

Mid-l~vel Management Presence

The inspector rioted the presence of mid-level management at

"Vision through Quality" sessions and tailgate meetings .. However,

minimal interaction betweeh mid-level management and Dresden

personnel at th~ actual job-site or duty station was not~d. *

b.

B.us 34-:-2 Temporary Alteration

On March I9, 1992, temporary alteration (T/A) III-7-92 installed

-measuring and test equipment (M&TE) on the auxiliary compart~ent

of ESF 4I60-volt AC Bus 34-1 to monitor voltage. This T/A

provided an indirect interface between Class IE safety related

electrical equipment and non-safety equipment.

The IO CFR 50.59 .

safety evaluation concluded the change would not affect any .

operating modes or eq~ipment failures.

The technical e~aluation

concluded safety related equipment was affected by the T/A.

However, *the safety evaluation did Tiot address the probability or

consequences of malfunctioning M&TE or how the Class IE circuit

would be protected followihg a malfun~tion of the M&TE .

. A previous rion-cit~d:violation (50-237/910I6-0I(DRP)) was issued

for the failure t6 adequately considered the effect rif a

malfunction of non"".safety equipment on a safety related syste*m.

In this tase a T/A

(TA"".II-7~091) on the Unit 2 high.pressure

coolant injection (HPCI) system provided an interface between

cl.ass IE safety related electrical equipment and non-safety M&TE.

The current Dresden licensing bases included a Systematic

Evaluation Program (SEP) commitment to incorporate the electtical

isolation philosophy of IEEE 384 and Regulatory Guide 1.75 fot

plant modifications whenever practical (1985 CECo letter from B.

21.

.

.

Rybak to R. Gilbert (NRR)).

The commitment to IEEE 384 and

potential failure modes of the M&TE,_ and the effect of those .

failure modes, should have been considered in the safety

~valuation process.

To-.address the violation, OAP I0-02, "IO CFR 50.59 Saf~ty

Evaluation/Scre~riing", was revised to incorporate a safety

evaluation screening review worksheet.

The work sheet asks if

safety-~elated class IE Bus integrity is maintained and if safety-

.* related circuits are isolated ~nd separated from non-safety~

related circuits. The safety evaluation preparer or reviewer did

not use the checklist and were not aware of the commitment t6 IEEE 384.

The reason why the corrective actions were not adequ~te* to

prevent recurrerice will be reviewed as yet another example .of

unresolved item (t37/92005-0I(DRP)).

c.

The inspector met wit~ the* orisite quality as~uranc~ g~oup and

discusied two performance based initiatives t~ determine present

p~rformance and the effectiveriess of recent management corrective

~ctions tb:station performance.

One of the initiatives involved

using senicir licensed personnel from other facilities to revie~

operator performance on a periodic basis.

The oth~r initiati~e

involved a soft-side evaluation of the most retent management

corrective action~. *Both initiatives tesulted in soft-side

  • assessments which support the inspector's observations outlined in

section 10.~ above.

.

.

No violations -or deviations ~ere identified; however another example of

~previously discussed unresolved-item was. mentibned.

ll~ . Mee~inqs and cith~r Activiti~s (36702)

-a.

On March'I9; I992, the Regional Administrator and st~ff met with *

CECo senior management at corporate headquarters in Downers Grove,

Illinois. *The meeting agenda included the licensee's *"Vision .

. through Quality" program, plant material cbnditions, engineering,

future "oldu plant (Dresden, Quad Cities and Zion) initiatives and.

design basis retri evabi 1 itf.

b~

On March 30, I992, a management me~ting was held iri the NRC

regional office. Attending the meeting wer~ mid-level NRC *

regional management, NRR project and IO CFR 50.59 technical

representatives and key CECo management personnel involved i~

training and approving 10 CFR 50.59 safety evaluati-0ns.

The

subject of the meeting was a safety evaluation performed by the

licensee to support control room habitability when discrepancies

in a past habitability ~ere discovered.

See unresolved item.

.

  • 237/90022-02 discussed in inspection reports 237/90022, 9I031, and

91039 for further details.

At the conclusion of the meeting the licensee acknowledged that

the NRC should have been contacted regarding the change in

22

. 12.

c.

assumptions associated with the most recent habitability an.alysis.

'

.

'

O~ March 30, 1992, the Division Director of Reactor Projetts ~et

with the.licensee's operations improvement team and select members

6f oper~tion~ ~anagement. *The meeting_entailed a dialogue from**

the director on safe operating philosophy and questions from the

team to the director on points of interest;

Unre~olved Ite~s .-

Unresolved items ~re matters about which more information is req~ired in

order to ascertain whether.they ar~ acceptable items, open* items,

violations, pr deviations. Unresolved items disclosed during this

inspection are discussed in sections 2.a, *2.c(l}, 4.b.l, 5.a, 6.b,.

7 .c(l), 7 .c(2), 9.a, 9.b~ 9.e and 10.b.

  • -

13.'

Open Items

Open items are matters which have been discussed with the licensee;

which will be r~vi~wed further by the inspector; and which involve some*

action on the part of the NRC, the licens~e. or both.

An Open item

disclosed d~ring this* inspection is discussed in Section 4.a.l.

14.

Exit Interview

The inspecto~s met with lic~nsee reptesentatives (denoted in section 1)

during th~ inspection period and at the conclusio~ of the inspectioh

period on April 10,. 1992 .. The inspectors summarized the scope and

  • re~ults of the insp~ction and. discussed the.likely content of this

inspection report.

The license~ acknowledged the.information and did

  • not indic~te that any of the information disclosed during the inspection

could be considered proprietary in nature.

.

.

23