ML17157C238

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Insp Repts 50-387/93-01 & 50-388/93-01 on 930101-0215. Violations Noted.Major Areas Inspected:Plant Operations, Radiation Protection,Surveillance & Maint & Safety Assessment/Quality Verification
ML17157C238
Person / Time
Site: Susquehanna  Talen Energy icon.png
Issue date: 03/05/1993
From: Jason White
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML17157C236 List:
References
50-387-93-01-01, 50-387-93-1, 50-387-93-1-1, 50-388-93-01, 50-388-93-1, NUDOCS 9303160054
Download: ML17157C238 (22)


See also: IR 05000387/1993001

Text

e

UNITED STATES NUCLEAR REGULATORY COMMISSION

REGION I

Inspection

Report Nos.

50-387/93-01; 50-388/93-01

License Nos.

NPF-14; NPF-22

Licensee;

Pennsylvania Power and Light Company

2.North Ninth Street

Allentown, Pennsylvania

18101

Facility Name:

Inspection At:

Susquehanna

Steam Electric Station

Salem Township, Pennsylvania

Inspection

Conducted:

January

1, 1993 - February 15, 1993

Inspectors:

G. S. Barber, Senior Resident Inspec

SSES

D. J. Mannai, Res't

tor,

Approved By:

J. Whi, Chief

Reac

r Projects Section No. 2A,

ate

Thi i

I '>>

d

i

d

i

i

p

(during day and backshift hours) of station activities, including: plant operations; radiation

protection; surveillance and maintenance;

and safety assessment/quality

verification.

One

violation was identified regarding tracking out-of-service times during instrumentation

surveillances

(Section 4.4.1 pertains).

Findings and conclusions of this inspection effort are

summarized in the Executive Summary.

Details are provided in the inspection report.

9303ib0054

930308

PDR

ADOCK 05000387

Q

PDR

EXECUTIVESUMMARY

Susquehanna

Inspection Reports

50-387/93-01; 50-388/93-01

January

1, 1993 - February 15,

1993'perations

(30702, 71707, 71710)

During the period, Unit 2 was shutdown to effect repairs to the main generator exciter.

During the plant shutdown administrative cooldown rate limits, as monitored at the

recirculation loop suction lines, were exceeded.

Administratively, the cooldown rate is

limited to (90'F/hr by station procedures., About 103'P/hr was measured

at the

recirculation loop suction lines.

The licensee determined that the Technical Specification

Limitof 100'F/hr was not exceeded

since the correct indicator for plant conditions, i.e.,

saturated reactor steam dome temperature

(Tsat) indicated less than 60 F/hr.

The inspector

concluded weak communications and control by operators resulted in exceeding the

administrative limits. The inspector also noted that operators did not fully understand which

temperature indicators are used to determine Technical Specification compliance.

Section

2.2.1 pertains.

During the period radwaste transformer OX340 faulted.

The transformer failure resulted in

an undervoltage condition that propagated to both Susquehanna

Units.

The voltage transient

caused isolations of several primary containment isolation (PCIS) valves.

Operators

promptly responded

to the event and rapidly restored systems to normal.

Nuclear System

Engineering (NSE) reviewed plant response.

NSE found that systems operated per design

and no anomalies were detected.'he

licensee determined the cause of the transformed fault

was water intrusion into the transformer cabinet;

The inspector identified that this was a

third instance of an electrical fault on a balance of plant system having an effect on class

"1E" safety related systems since 1989,

The licensee agreed to evaluate system

enhancements

to minimize the possibility of these occurrences.

The licensee's investigation

and final resolution was still in progress at the conclusion of the inspection period.

The

inspector willassess

licensee corrective actions during inspector review of the Licensee

Event Report.

Section 2.2.2 pertains.

Maintenance/Surveillance

(61726, 62703)

During a routine control room walkdown, the inspector observed the performance of an

instrumentation surveillance on the low-low-lowlevel reactor water trip channels.

By

Technical Specifications (TS), each channel could be made inoperable for a period of two

hours without tripping the channel.

The inspector determined that the licensee was not

adequately tracking each channel's out-of-service time.

The actual out-of-service time for

each individual channel is not known, however, licensee past practice indicates that the time

was likely less than two hours.

This is an apparent violation.

Section 4.4.1 pertains.

Engineering/Technical Support (71707, 92720; 93702)

The licensee identified a small pinhole leak in a fuel assembly based on an increase in Unit 2

offgas pretreatment radioactivity.

The leak is extremely small and does not result in

approaching any offsite dose limits. The licensee has comprehensive

procedures in place to

address

any increases in radioactivity.

The fuel vendor willperform fuel sipping at the next

refueling outage to identify and repair the leaky fuel assembly.

The licensee's actions were

conservative and comprehensive.

Section 7.2.1 pertains;

The licensee identified an inconsistency in the piping analysis used to predict stresses

during

a high energy line, break on the Reactor Water Cleanup (RWCU) system.

A 45 degree angle

restraint was used in place of a vertical restraint for an elbow downstream of the RWCU

outboard containment isolation valve.

Bechtel was contacted and reran the analysis with

satisfactory results.

The inspector questioned

the licensee to ensure that the assumptions

used in the original analysis were also used for re-analyses.

Bechtel assured

the licensee that

all of the original assumptions were used, and the minor model changes did not invalidate the

results.

The inspector noted the licensee's identification of this discrepancy

as a positive

initiative. Section 7.2.2 pertains.

Safety Assessment/Assurance

of Quality (40500, 90712, 92700, 92701)

The inspector reviewed three Licensee Event Reports during the period.

Section 8.1

pertains.

TABLEOF CONTENTS

EXECUTIVE SUMMARY

SUMMARYOF OPERATIONS.......

1.1

Inspection Activities..........

1.2

Susquehanna

Unit 1 Summary....

1.3

Susquehanna

Unit 2 Summary....

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2.

PERATIONS

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2.1

Inspection Activities................................

2.2

Inspection Findings and Review of Events

2.2.1

Administrative Cooldown Rate Exceeded During Plant Shutdown

2.2.2

Engineered Safety Feature Actuation Due to Transformer Fault

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3.

RADIOLOGICALCONTROLS

3.1

Inspection Activities..... ~........ ~....

3.2

Inspection Findings

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4.

MAINTENANCE/SURVEILLANCE

4.1

Maintenance and Surveillance Inspection Activity .

4.2

Maintenance Observations

4.3

Surveillance Observations

4,4

Inspection Findings

4.4.1

Reactor Water Level Surveillance Concerns

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5.

EMERGENCY PREPAREDNESS

5.1

Inspection Activity......................

5.2

Inspection Findings

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6.

SECURITY

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Inspection Activity............

6.2

Inspection Findings

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8.

ENGINEERING/TECHNICALSUPPORT

7.1

Inspection Activity............ ~............

7.2

Inspection Findings

7.2.1

Long Term Fuel Performance Monitoring - Unit 2

7.2.2

Excessive Piping Stresses During High Energy Line

SAFETY ASSESSMENT/QUALITY VERIFICATION..

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Licensee Event Reports..................

8..2

Open Items

Breaks

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'ANAGEMENTAND EXIT MEETINGS ..........

9.1

Resident Exit and Periodic Meetings........

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Inspections Conducted-By Region Based Inspectors

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111

1.

SUMMARYOF OPERATIONS

1.1

Inspection Activities

The purpose of this inspection was to assess

licensee activities at Susquehanna

Steam Electric

Station (SSES) as they related to reactor safety and worker radiation protection.

Within,each

inspection area, the inspectors documented the specific purpose of the area under review, the

scope of-inspection activities and findings, along with appropriate conclusions.

This

assessment

is based on actual observation of licensee activities,'nterviews with licensee

personnel,

measurement of radiation levels, independent calculation, and selective review of

applicable documents.

Abbreviations are used throughout the text.

Attachment

1 provides a'listing of these

abbreviations.

1.2

Susquehanna

Unit 1 Summary

Unit 1 operated at or near full power for the duration of the inspection period.

Operators

conducted several routine power reductions during the period to facilitate control rod pattern'

adjustments,

surveillance testing, and maintenance.

One unplanned ESF actuation occurred

due to a volta'ge transient caused by a nonsafety related transformer failure,

Section 2.2.2

pertains.

1.3

Susquehanna

Unit 2 Surmnary

Unit 2 began the inspection period at 100% power.

On January 29, power was reduced to

60% to repair a condenser water box tube leak.

During the down power, a generator exciter

field ground alarm was received.

After investigation, the licensee identified the need for a

plant shutdown to determine and correct the cause of the ground.

The unit reached

Condition 4 at 10:20 a.m. on February

1. During the cooldown, operators

exceeded

administrative cooldown limits. Section 2.2.1 pertains.

On February 5, following the

generator exciter repair, the unit was started up.

The unit returned to 100% power operation

on February 8. Two unplanned ESF actuations occurred during the period.

One was caused

by the transformer failure, which resulted in primary containment isolations.

Section 2.2.2

pertains,

The other unplanned ESF actuation occurred during a momentary loss of 120 volt

AC instrument power.

Several primary containment isolations occurred as a result of the

voltage transient.

Section 8.1 pertains.

2.

OPERATIONS

2.1

Inspection Activities

The inspectors verified that the facility was operated safely and in conformance with

regulatory requirements.

Pennsylvania Power and Light {PP&L) Company management

control was evaluated by direct observation of activities, tours of the facility, interviews and

discussions with personnel,

independent verification of safety system status and Limiting

,Conditions for Operation, and review of facility records.

These inspection. activities were

conducted in accordance with NRC inspection procedure 71707.

The inspector determined

that Unit 1 operational and Unit 2 outage activities were conducted safely during this period.

I

The inspectors performed 4.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> of deep backshift inspections during the period.

These

deep backshift inspections covered licensee activities during between

10:00 p.m. and 6:00

a.m. on weekdays,

and weekends and holidays.

2.2

Inspection Findings and Review of Events

2.2.1

Administrative Cooldown-Rate Exceeded During Plant Shutdown

On February

1, Unit 2 was shutdown to repair the main generator exciter.

During the

shutdown, the cooldown rate as measured

at the "A" recirculation loop suction line was

about 103'F per hour.

This, rate exceed the licensee's administrative limitof less that 90'F

per hour.

The administrative limitwas established

to assure that the Technical Specification

(TS) Limitof 100'F per hour cooldown is not exceeded.

Later analysis, revealed that the

saturated

steam dome temperature

(the approved indicator for the existing plant conditions

for assuring compliance with Technical Specification (TS) 3.4.6.1) indicated a cooldown rate

of about 60'F per hour.

Notwithstanding, the operators took appropriate action to reduce

the cooldown rate at the recirculation suction line to within the administrative limit. The

licensee documented

this occurrence in Significant Operating Occurrence Report (SOOR) 93-

024.

The plant was being taken to cold shutdown following GO-200-005, "Plant Shutdown to Cold

Shutdown."

The operators used SO-200-011, Reactor Vessel Temperature and Pressure

Recording, to record temperatures

and determine cooldown rate every fifteen minutes.

GO-

200-005 requires that the cooldown rate be limited to 90'F/hour.

SO-200-011 requires

action be taken to reduce the cooldown rate iftemperature

change is >25'F in a fifteen

minute period.

The temperatures

monitored are recirculation Loop "A" suction line,

recirculation Loop "B" suction line, reactor vessel bottom head drain and reactor steam

dome'emperatures.

After determining a fifteen minute cooldown rate of 33'F on the "A"

recirculation suction line, operators took action to reduce the cooldown rate.

However, the

cooldown rate exceeded

100'F in one hour on the "A" recirculation suction line.

SO-200-

011 requires that TS 3.4.6.1 be entered only ifreactor steam dome temperature delta-T's are

greater than 100'F in any one hour.

The inspector questioned why operations entered the

TS action statement when the procedure did not require it. The inspector determined that the

TS action statement was entered

as a prudency measure until Nuclear System Engineering

could complete their evaluation.

From earlier analysis of excessive cooldown rate events, the licensee, in concert with

General Electric, determined the 100'F limit specifically applies to the belt line region of the

reactor vessel relative to brittle fracture prevention.

The analysis showed that reactor belt

line temperature is best determined from reactor steam dome temperature

(Tsat) with coolant

temperature )212'F. Ifcoolant temperature is less than 212'F then reactor recirculation

suction line temperatures

are used.

The lowest coolant temperature at the time of the event

was 224'F.

The GE analysis also indicated that non-beltline regions have been analyzed for

the most severe applicable design basis thermal event and are not limiting. Therefore, they

do not require monitoring to ensure TS compliance.

The NRC accepted this method of

determining compliance with TS cooldown rate limits and documented

acceptance

in

Inspection Report 50-387/91-18.

Maximum change in Tsat during the event was less than

60'F in one hour.

The licensee decided that no TS limits were exceeded

and pressure

temperature curve limits were not challenged.

Nuclear System Engineering (NSE)

determined that the cooldown observed on the "A" recirculation loop was not detrimental to

the recirculation piping or reactor vessel.

The inspector agreed with the licensee determination that no TS limits were exceeded.

The

licensee conservatively performed an engineering evaluation though one was not required.

The inspector determined inadequate communications and control between the operator

controlling the cooldown and the operator recording the temperatures

resulted in exceeding

administrative cooldown limits. Aside from following the procedure, no prior specific

discussions took place between the unit supervisor (SRO) and the plant control operator (RO)

to outline what actions would be taken to ensure cooldown rates would not be exceeded.

The

inspector concluded that, even though the procedure was very specific, the temperature

indication that should be used to determine compliance with the TS cooldown rate limitwas

not well understood by operators.

Licensee actions to prevent recurrence willconsist of reviewing this event with all operations

shifts,

Additionally, the basis for the temperature indication to be used for determining TS

compliance willbe discussed.

The licensee willemphasize the need for a pre-evolution brief

(tailboard) for significant plant evolutions.

2.2.2

Engineered Safety Feature Actuation Due to Transformer Fault

On February

1, a non-safety related radwaste transformer, OX340, (normal feed to radwaste

load center 08340) faulted, resulting in an undervoltage condition that propagated to both

Susquehanna

units.. At the time, Unit 1 was at 100% power, Unit 2 was in Condition 4,

Cold Shutdown.

Failure of transformer OX340 tripped the 13.8kv feeder breaker that feeds

the radwaste load center and two Unit 2 turbine building heating load centers.

The licensee

restored all three 480 volt load center's on alternate power supplies.

4

The undervoltage condition was of sufficient magnitude and duration to cause isolation of

several primary containment isolation system (PCIS) valves.

Systems affected included

containment atmospheric control (CAC) valves and containment- instrument gas (CIG) valves.

This constituted an unplanned Engineered Safety Feature (ESF) actuation.

The licensee

found the ESF actuations to be invalid but reportable per 10 CFR 50.72.

The licensee made

the required four hour NRC notification.

Besides numerous alarms, annunciators

and loss of

Balance of Plant (BOP) equipment, Unit 2 Reactor Water Cleanup (RWCU) and fuel pool

cooling (FPC) pumps stopped due to the low voltage condition.

Operators promptly restored important systems to service.

Operations personnel documented

observations'nd

plant system'responses.

Nuclear System Engineering (NSE) began a review

of observations

and plant responses

to ensure all systems functioned per design.-

Until protective undervoltage relaying tripped the transformer feeder breaker, the

undervoltage transient propagated

to Startup Bus 20 which is fed from transformer T-20.

Startup Bus 20 is common to both units.

Division 2 4kv emergency

busses

are supplied from

Startup Bus 20 for both units.

The resultant transient effects were explainable.

The licensee

deteimined,

based on a review of the event and operator observations,

that no anomalies

existed in plant response.

The licensee determined the transformer failure was due to water intrusion into the load

center transformer cabinet.

NSE found water dripping from inside the exhaust'ucting from

radwaste tank vent filtered exhaust fan discharge, to the turbine building exhaust vent on the

top of the electrical cabinet.

The ductwork is located above the load center transformer

cabinet.

The licensee made immediate provisions to collect the leaking water to prevent

additional intrusion in the electrical cabinet. >NSE preliminarily determined condensation of

moisture entrained in the air inside the ductwork was the source of the water dripping from

inside the ductwork.

Licensee investigation, analysis and evaluation of water coming from

the d'uctwork was in progress at the conclusion~of the inspection period.

i

I

The inspector concluded that the operators promptly and properly responded to the

transformer failure and resultant plant perturbations.

PP&L used experience gained from a

similar previous occurrence to quickly understand

the effects of the voltage transient and

rapidly restored plant systems to a normal configuration.

The inspector agreed with the-

utility'-s reportability determination.

Of particular strength was Nuclear System

  • Engineering's approach to reviewing all operations personnel observations

and documenting

plant effects to ensure that systems operated

as designed.

NSE concluded all plant responses

were explainable and that no anomalies were detected.

The inspector noted that this.was a third occurrence since 1989 of an electrical fault on a

- Balance of.Plant (BOP) system that affected safety-related

class "1E" equipment.

The

previous occurrences

are documented in SOORs 1-89-341 and 1-89-043.

The licensee agreed

to review the need for system enhancements

to minimize BOP system faults from affecting

class "lE" safety related systems.

Licensee resolution of the event was still in progress at

0

'the conclusion of the inspection period.

The inspector willreview final licensee actions to

prevent recurrence

and cause determinations during review of the Licensee Event Report

(LER).

3.

RADIOLOGICALCONTROLS

3.1

Inspection Activities

PP&L's compliance with the radiological protection program was verified on a periodic

basis.

These inspection activities were conducted in accordance with NRC inspection

procedure 71707.

3.2

Inspection Findings

Observations of radiological controls during maintenance activities and plant tours indicated

that workers generally obeyed postings and Radiation Work Permit requirements.

4.

MAINTENANCE/SURVEILLANCE

4.1

Maintenance and Surveillance Inspection Activity

On a sampling basis, the inspector observed and/or reviewed selected surveillance and

maintenance activities to ensure that specific programmatic elements described below were

being met.

Details of this review are documented in the following sections.

4.2

Maintenance Observations

The inspector observed and/or reviewed selected maintenance activities to determine that the

work was conducted in accordance with approved procedures,

regulatory guides, Technical

Specifications, and industry codes or standards.

The following items were considered,

as

applicable, during this review: Limiting Conditions for Operation were met while

components or systems were removed from service; required administrative approvals were

obtained prior to initiating the work; activities were accomplished using approved procedures

and quality control hold points were established where required; functional testing was

performed prior to declaring the involved component(s) operable; activities were

accomplished by qualified personnel; radiological controls were implemented; fire protection

controls were implemented; and the equipment was verified to be properly returned to

service.

These observations and/or reviews included:

WA 15083, Test Equipment Installation for "D" Emergency Diesel Generator (EDG)

Emergency Service Water (ESW) Hydrostatic Test, dated January 25.

0

WA 24884, Core Spray Pump Minimum Flow Valve HV-152F013A Breaker

Maintenance,

dated January 27.

WA 23414, Install Sample Point and Sample Station for the "D" Emergency Diesel

Generator,

dated January 28.

WA 05401, HPCI Auxiliary Lube Oil Pump replacement,

dated February 4.

4.3

- Surveillance Observations

The inspector observed and/or reviewed the following surveillance test to determine that the

following criteria, ifapplicable to the specific test, were met:

the test conformed to

Technical Specification requirements;

administrative approvals and tagouts were obtained

before initiating the surveillance; testing was accomplished by qualified personnel in

accordance with an approved procedure;

test instrumentation was calibrated; Limiting

Conditions for Operations were met; test data was accurate and complete; removal and

restoration of the affected components

was properly accomplished;

test results met Technical

Specification and procedural requirements;

deficiencies noted were reviewed and

appropriately resolved; and the surveillance was completed at the required frequency.

SI-280-303,

18 Month Calibration of Reactor Vessel Water Level Channels LIS-B21-

2N031 A,B,C,D, dated February 9.

4.4

Inspection Findings

The inspector reviewed the listed surveillance activity. The review noted that work was

properly released before its commencement.

However, concerns arose on the licensee's

method of verifying compliance with Technical Specifications.

Section 4.4.1 pertains.

4.4.1

Reactor Water Level Surveillance Concerns

On February 8, during a routine control room walkdown, the inspector observed the

performance of 18 month calibration of the reactor water level-low-low-lowtrip channels

(Level 1) per surveillance procedure, SI-280-303.

The inspector noted that the Unit 2

Limiting Condition for Operation (LCO) log contained no entry for this surveillance activity.

Consequently,

the inspector questioned the unit supervisor (US).

The US indicated that a

Nuclear Department Administrative'rocedure (NDAP-QA-722, Step 6.7.1) allowed certain

safety-related instruments to be removed from service without being declared inoperable.

The inspector questioned the validity of this procedure step since SI-280-303 required

isolation of each trip channel in sequence.

The inspector noted that when the instrument is

isolated, it is no longer be capable of detecting an actual low reactor water level condition,

and would not perform its intended safety function.

-

Based on this discussion,

the US agreed that the instrument was inoperable and that the

procedure was poorly worded.

However, he stated it was the responsibility of the work

group to track the out-of-service times.

The inspector noted that the procedure suggested,

but did not require, the work group to monitor and control out-of-service times for the

individual channels;

and, did not recognize or address

the responsibility of licensed operators

to track the status of inoperable equipment in accordance with NDAP-QA-302, System Status

and Equipment Control.

NDAP-QA-302, Step 6.3.2 requires that shift supervision make

,LCO log entries whenever equipment is made or found to be inoperable.

The licensee did

not make the required LCO entries when the four Level

1 trip channels were intentionally

made inoperable per SI-280-303.

The inspector noted that this requirement could have been

accommodated

had the work group actually logged- and tracked the out-of-service times for

each channel.

On February

10, the inspector reviewed the completed surveillance on the Level

1 trip

switches (SI-280-303) and rioted that the work group did not track the times that the various

'instruments were taken out of and returned to service.

NDAP-QA-722, Step 6.7.4 only

suggests

that start and stop times be documented.

Technical Specification (TS) 3.3.3, Table

3.3.3-1, footnote (a) allows channels to be made inoperable for a period not exceeding two

hours without tripping the affected channel as long as the redundant channel in the same trip

system is operable.

For example, the "A" channel could be isolated and surveilled without

tripping Division 1 of the Reactor Protection System (RPS) as long as the "C" channel was

operable and capable of providing the necessary Division 1 safety functions on an actual low

level condition.

This would allow the surveillance to be completed without a half

scram'ignal

present,

thereby reducing the overall complexity of the surveillance,

However', such

action required the licensee to assure that the subject instr'uments were not out-of-service for

an excessive period without tripping the affected channel.

The inspector noted that the TS

action required initiating plant shutdown with less the minimum (2) channels operable.

The inspector noted that the tracking of out-of-service times, as practiced by the licensee,

was inadequate to assure compliance with the applicable Technical Specification.

Start and

stop times were not documented per NDAP-QA-722. The inspector noted that failure to

document specific start and stop times prevented monitoring and verification of the

acceptability of SI-280-303 relative to meeting the performance standard.

The inspector

determined that SI-280-303 commenced at 10:45 a.m., February 8, and ended at 8:50 a.m.,

February 9, a period of 22 hours2.546296e-4 days <br />0.00611 hours <br />3.637566e-5 weeks <br />8.371e-6 months <br />.

The inspector determined that there was no other record

or system that provided assurance

that the out-of-service times were effectively monitored

and controlled.

Within the 22 hour2.546296e-4 days <br />0.00611 hours <br />3.637566e-5 weeks <br />8.371e-6 months <br /> period, it is not known how long each individual channel

was actually out-of-service.

However, based on interviews with operators and Instrument

and Control personnel,

past practice indicates that individual channels are typically out-of-

service for no more than 30 minutes for this surveillance, and only one channel at a time is

actually affected.

Notwithstanding, the inability of the licensee to show compliance with TS 3.'3.3 is an

apparent violation of 10 CFR 50, Appendix B, Criterion V which requires that procedures

be

written to ensure that specific quantitative and qualitative information be provided to

demonstrate

satisfactory accomplishment.

In this case, the lack of a requirement to

specifically monitor and control out-of-service times for the reactor water level indicators

while in surveillance in accordance with TS 3.3.3, constitutes the bases for this apparent

violation. (VIO 50-388/93-01-01)

Upon identification by the inspector, the licensee took prompt actions to rectify this apparent

violation. The licensee immediately initiated action to track each individual instrument

channel's out-of-service time on the surveillance procedure cover sheet in the control room;

and required shift supervision approval prior to taking any instrumentation channel out-of-

service during the surveillance.

The licensee agreed

to=use this work practice for all future

surveillance that allowed making a channel inoperable without tripping.

5.

EMERGENCY PREPAREDNESS

5.1

Inspection Activity

The inspector reviewed licensee event notifications and reporting requirements for events that

could have required entry into the emergency plan.

5.2

Inspection Findings

No events were identified that required emergency plan entry. No inadequacies

were

identified.

6.

SECURITY

6.1

Inspection Activity

PP&L's implementation of the physical security program was verified on'a periodic basis,

including the adequacy of staffing, entry control, alarm stations, and physical boundaries.

These inspection activities were conducted in accordance with NRC inspection procedure

71707.

6.2

Inspection Findings

The inspector reviewed access

and egress controls throughout the period.'o unacceptable

conditions were noted.

7.

ENGINEERING/TECHNICALSUPPORT

7.1

Inspection Activity

The inspector periodically reviewed engineering and technical support activities during this

inspection period.

The on-site Nuclear Systems Engineering (NSE) organization, along with

Nuclear Technology (NPE) in Allentown, provided engineering resolution for problems

during the inspection period.

NSE generally addressed

the short term resolution of

engineering problems; and interfaced with the Nuclear Modifications organization to schedule

modifications and design changes,

as appropriate, to provide long term corrective action.

The inspector verified that problem resolutions were thorough and directed at preventing

recurrences.

In addition, the inspector reviewed short term actions to ensure that they

provided reasonable

assurance

that safe operation could be maintained.

7.2

Inspection Findings

7.2.1

Long Term Fuel Performance Monitoring - Unit 2

The licensee monitors fuel performance on an ongoing basis for both units.

On December

15, the licensee detected

a slightly elevated sample in the Unit 2 offgas pretreatment

stream.

Pretreatment activity increased from approximately 100 uci/sec to approximately 170 uci/sec.

Normally, this type of change might have been within the bounds of expected activities.

However, Unit 2 activity had been trending downward since starting up from the fifth

refueling outage on November 24 before itjumped on December

15.

As a result, the

licensee intensified their fuel performance monitoring.

The licensee determined that the most likely cause for the increased pretreatment activity was

a pinhole leak in a once-burned fuel assembly.

They concluded this based on the existing

Cs-134 to Cs-137 ratios which also ruled out either new fuel or highly exposed reinserted

fuel (fuel used to support their exposure extension program).

On January 30, the licensee began shut down of Unit 2 and observed no unexpected

changes

in offgas pretreatment levels.

A sample taken on the subsequent

startup on February 7

confirmed the continued presence of the leak, and subsequent

pretreatment

samples indicated

the leak did not worsen.

The licensee willcontinue to monitor this minor leak and expects some continued degradation

due to secondary hydriding.

Detailed procedures exist that identify specific action levels

relative to any increase in offgas activity. These procedures provide a graded response

commensurate

with the actual activity level.

The inspector questioned the licensee in detail on their actions in response to this extremely

small fuel leak.

The inspector noted that the actual activity of approximately 170 uci/sec is a

small fraction of the 3000 uci/sec seen during a previous leak.

He also noted the licensee's

10

monitoring program was conservative and comprehensive.

In response to inspector

questioning, the licensee initiated a SOOR to track this activity until the leaky bundle is

identified during the next refueling outage.

The fuel vendor has been contacted and has

agreed to identify the leaker by using fuel sipping.

The inspector found the licensee's

response

to this issue to be effective and thorough.

ll

7.2.2

Excessive Hying Stresses During High Energy Line Breaks

The licensee identified the potential for excessive piping stresses

during a postulated High

Energy Line Break (HELB). 'As part of their Design Basis Documentation (DBD), the

licensee reviewed the ability of certain pipe supports to limitpipe stresses

to acceptable

valves during a HELB. They determined that the pipe break analysis model for the Reactor

Water Cleanup (RWCU) system may have been non-conservative;

Specifically, the RWCU

outboard containment isolation (F004) valve was assumed to have been confined by a vertical

restraint (PR 97Aa) when in actuality it was installed on a 45 degree angle.

The installed

angle introduced a new force component that was unaccounted for in the original analysis.

As a result, the licensee issued Engineering Discrepancy Report (EDR) G30007 to resolve

this concern.

The licensee contacted Bechtel on January 27 to rerun the original piping analysis with the

installed configuration.

Bechtel obtained the original computer model and a version of the

ANSYS program used for the original model on January 29.

The model was benchm'arked

on January 31.

The proper restraint configuration was installed in the model and study runs

were conducted.

The study runs were completed on February 6 and showed that the stress

levels on the piping were acceptable.

If

The inspector monitored the licensee's actions in this specific area throughout the inspection

period, and reviewed apparent changes relative to the original design assumptions.

Such

changes included the accommodation of the 45;degree pipe restraint, and the proper

-.

accounting of frictional forces that would be applied to the pipe elbow after impact with the

restraint during the postulated HELB. The inspector concluded that these minor adjustments

were appropriate and did not appear to exceed the regulatory bounds of the original analysis.

The inspector had no further questions on this issue.

8.

SAFETY ASSESSMFAT/QUALITYVEIUPICATION

8.1

Licensee Event Reports

The inspector reviewed LERs to verify that details of the event were clearly reported,

including the accuracy of the description of the'cause

and the adequacy of corrective action,

The inspector determined whether further information was required from the licensee,

whether generic implications were involved, and whether the event warranted onsite

followup. The following LERs were reviewed:

11

Unit 1

92-010-00

"Offgas Guard Bed "B" Experienced Elevated Temperatures"

On June 13, 1992 with Unit 1 in Condition 2 at 2% power, the "1B" guard bed experienced

a temperature excursion'fter purging the guard bed with heated air and during an air purge

of the Unit 1 offgas,recombiner.

The licensee determined that the condition was not

reportable, but submitted a voluntary LER to provide information to the NRC. The inspector

agreed with the licensee's reportability analysis.

NRC Inspection Report 50-387/92-16

reviewed this event.

The LER was acceptable,

92-014-00

Manufacturer's Installation and Operations Manual: Required Incorrect

'O'ing Lubricants for, Solenoid Valves

On September 9, 1992 during an evaluation of NRC Generic Letter 91-15, PP&L engineers

became aware that station circle seal solenoid valves (SOV's) could be susceptible to

deterioration of their '0'ings.

The concern was due to the incompatibility of hydrocarbons

(petroleum jelly) with ethylene propylene elastomers

(o-rings).

Circle Seal installation and

operations manual (IOM) recommend

use of petroleum jelly. Although the licensee

determined the event was not reportable,

a voluntary LER was submitted to provide

information to the NRC.

The inspector agreed with the licensee's reportability

determination,

NRC Inspection Report 50-387/92-22 reviewed this event,

The LER was

acceptable.

Unit 2

93-001-00

Momentary Loss of 120 VAC Instrument Power Resulted in Invalid ESF

Actuations

At 6:25 a.m. on January

14, 1993, with Unit 2 in Condition

1 at 100% power,.the alarm for

Instrument AC Panel 2Y226 Power Failure was received in the control room.

Invalid

Engineered Safety Feature (ESF) actuations occurred as containment isolations of the Reactor

Water Cleanup System, "B" Loop of Containment Atmosphere Control and Drywell Floor

Drain Sump lines.

The cause for the initial Instrument AC Panel 2Y226 Power Failure

alarm and the momentary voltage dip to the subject loads on Panel 2Y226 which resulted in

the invalid ESF actuations was attributed to failure of a rectifier on the Loss of Voltage

Relay located in Panel 2Y226.

The licensee considered the failure to be an isolated

occurrence.

System response to the momentary voltage dip of the 120 VAC power was per

design.

Per 10 CFR 50.73, invalid ESF actuations of the RWCU system are exempt from the ESF

reporting requirement.

However, invalid ESF actuations of the CAC and Reactor Building

Drain Sump isolation valves are not exempt from the ESF reporting criteria.

The LER was acceptable.

12

8.2

Open Items

(Update) VIO 50-387/92-23-01, Inadequate Inspection of Kaowool Fire Wrap

In Inspection Report 50-387/92-23, the inspector identified that the licensee did not inspect

Kaowool fire wrap as required by Technical Specification (TS) 3.7.7.

This conclusion was

reached after questioning mechanical maintenance personnel that performed the most recent

surveillance inspection.

They indicated that they only inspected Thermo-Lag and did not

inspect any Kaowool fire wrap.

This provided the basis for this apparent violation.

On January

19, during the fire protection enforcement conference,

the licensee disputed the

duration of this violation. They stated that Kaowool had been inspected per TS 3.7.7 from

initial licensing until December

1989 when a procedure change obscured the need for

continued Kaowool inspections.

The previous procedure methodology (pre-1990) identified

the fire wrap to be inspected by location (elevation and plant area) and by raceway number.

These raceways included both Thermo-Lag and Kaowool. The new methodology only

identified fire wrap locations and not raceways.

The briefings and training conducted by the

licensee were inadequate to cope with this new, limited procedural guidance.

Thus, only the

most recent inspections inadvertently omitted Kaowool.

On January 20 and 21, the inspector verified that the pre-1990'procedures

did include

Kaowool on the listings of fire wrap to be inspected.

In addition, the inspector sampled

certain in plant locations using the old procedure and verified that Kaowool did exist at these

locations.

A review of three pre-1990 inspections showed that licensee personnel inspected

raceways containing Kaowool.

Based on the above, the inspector concurred with the licensee

assertion on the violation duration.

The last valid Kaowool inspection preceded

the

procedure changes

made in December

1989, and it appeared

that removing the raceway

identifiers contributed to this apparent violation. The licensee is still in the process of

finalizing their corrective action.

This item is updated.

9.

MANAGEMENTAND EXITMEETINGS

9.1

Resident Exit and Periodic Meetings

The inspector discussed

the findings of this inspection with station management

throughout

and at the conclusion of the inspection period.

Based on NRC Region I review of this report

and discussions

held with licensee representatives,

it was determined that this report does not

contain information subject to 10 CFR 2.790 restrictions.

13

9.2

Inspections Conducted By Region Based Inspectors

1/12-1/13

EOPs

Immhan

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93-02

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H. Williams

14

ATI'ACHMENT 1

A rv>> nLi

AD

ADS

ANSI

ASME

CAC

CFR

CIG

CRDM

CREOASS

DG

DX

ECCS

EDR

EP

EPA

EQ

ERT

ESF

ESW

EWR

FO

FSAR

HVAC

IERP

ILRT

I&C

Jlo

LCO

LER

LLRT

LOCA

LOOP

MSIV

NCR

NDI

NPE

NPO

NQA

NRC

NSE

- Administrative Procedure

- Automatic Depressurization

System

- American Nuclear Standards Institute

- American Society of Mechanical Engineers

- Containment Atmosphere Control

- Code of Federal Regulations

- Containment Instrument Gas

- Control Rod Drive Mechanism

- Control Room Emergency Outside Air Supply System

- Diesel Generator

- Direct Expansion

- Emergency Core Cooling System

- Engineering Discrepancy Report

- Emergency Preparedness

- Electrical Protection Assembly

- Environmental Qualification

- Event Review Team

- Engineered Safety Features

- Emergency Service Water

- Engineering Work Request

- Fuel Oil

- Final Safety Analysis Report

- Heating, Ventilation, and Air Conditioning

- Industry Event Review Program

- Integrated Leak Rate Test

- Instrumentation and Control

- Justifications for Interim Operation

- Limiting Condition for Operation

- Licensee Event Report

- Local Leak Rate Test

- Loss of Coolant Accident

- Loss of Offsite Power

- Main Steam Isolation Valve

- Non Conformance Report

- Nuclear Department Instruction

- Nuclear Plant Engineering

- Nuclear Plant Operator

- Nuclear Quality Assurance

- Nuclear Regulatory Commission

- Nuclear Systems Engineering

15

OI

OOS

PC

PCIS

PMR

PORC

PSID

QA

RB

RBCCW

RCIC

RG

RHR

RHRSW

RPS

'RWCU

SGTS

SI

SO

SOOR

SPDS

SPING

TS

TSC

WA

Open Item

Out-of-Service

Protective Clothing

Primary Containment Isolation System

Plant Modification Request

Plant Operations Review Committee

Pounds Per Square Inch Differential

Quality Assurance

Reactor Building

Reactor Building Closed Cooling Water

Reactor Core Isolation Cooling

Regulatory Guide

Residual Heat Removal

Residual Heat Removal Service Water

Reactor Protection System

Reactor Water Cleanup

Standby Gas Treatment System

Surveillance Procedure,

Instrumentation and Control

Surveillance Procedure,

Operations

Significant Operating Occurrence Report

Safety Parameter Display System

Sample Particulate, Iodine, and Noble Gas

Technical Specifications

Technical Support Center

Work Authorization