ML17059C125
| ML17059C125 | |
| Person / Time | |
|---|---|
| Site: | Nine Mile Point |
| Issue date: | 07/07/1998 |
| From: | Doerflein L NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML17059C123 | List: |
| References | |
| 50-220-98-05, 50-220-98-5, 50-410-98-05, 50-410-98-5, NUDOCS 9807140059 | |
| Download: ML17059C125 (80) | |
See also: IR 05000220/1998005
Text
U.S. NUCLEAR REGULATORY COMMISSION
REGION I
Docket/Report Nos.:
50-220/98-05
50-41 0/98-05
License Nos.:
NPF-69
Licensee:
Niagara'ohawk Power Corporation
P. O. Box 63
Lycomnin, NY 13093
Facility:
Nine Mile Point, Units
1 and 2
Location:
Scriba, New York
Dates:
April 12 - May 23, 1998
Inspectors:
B. S.
T. A.
J. G.
L. A.
R. C.
R. A.
Norris, Senior Resident Inspector
Beltz, Resident Inspector
England, Reactor Engineer
Peluso, Radiation Specialist
'Ragland, Radiation Specialist
Skokowski, Resident Inspector
'I
Approved by:
Lawrence T. Doerflein, Chief
Projects Branch
1
Division of Reactor Projects
9807i4005980707
- DOCK 05000220
G
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TABLE OF CONTENTS
page
TABLE OF CONTENTS
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EXECUTIVE SUMMARY
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IV
SUMMARYOF ACTIVITIES...: .
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Niagara Mohawk Power Corporation (NMPC) Activities
Nuclear Regulatory Commission (NRC) Staff Activities ..
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II. MAINTENANCE ...... ~... ~... ~....................
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Conduct of Maintenance........................
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M1.1
General Comments................ ~........ ~...
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M8
Miscellaneous Maintenance Issues..........................
M8.1
(Closed) URI 50-220/96-01-03:
Inadequate Testing of Unit 1
Control Room Annunciators.... ~..........
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M8.2
(Closed) URI 50-410/96-10-01:
Post-Maintenance
Testing of
the Unit 2 Main Steam Line Radiation Monitors ... ~........
M8.3
(Closed) VIO 50-410/96-10-03:
Procedure Changes Not in
Accordance with TS Requirements
M8.4
(Closed) VIO 50-410/97-02-02:
Missed Unit 2 HPCS Actuation
, Instrumentation TS Surveillance Test ...................
M8.5
(Closed) LER 50-410/98-09:
Missed Battery TSSR Due to
Inappropriate Interpretation.
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I. OPERATIONS
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Conduct of Operations ......,,......................;......
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01.1
General Comments...................................
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01.2
Unit 1 - Failure to Follow Surveillance Test Procedure ~..........
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01.3
Conduct of Unit 2 Core Off-load Operations (60710) ...........
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01.4
Dropped Double Blade Guide During Unit 2 Off-load Operation .... 3
08
Miscellaneous Operations Issues .............."...........
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08.1
(Closed) LER 50-410/98-05:
Reactor Water Cleanup Isolation
on High Differential Flow Caused by Relief Valve Lifting......
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08.2
(Closed) LER 50-410/98-06:
Engineered Safety Feature Actuations
Due to Partial Loss of Offsite Power
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08.3
(Closed) LER 50-410/98-08;
HPCS Out of Service with One
Division of RHS in Suppression
Pool Cooling .......
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III. ENGINEERING..........
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E1
Conduct of Engineering......... ~.......,
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E1.1
General Comments..... '........
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E1.2
Unit 2 Emergency Diesel Generator Fuel Line
E3
Engineering Procedures
and Documentation
E3.1
Unit 2 ECCS Suction Strainer Modification
Leak ..........
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Table of Contents (cont'd)
E8
Miscellaneous Engineering Issues................. ~............ ~... 14
E8.1
(Closed) VIO 50-220 5, 50-410/96-01-05:
Failure to Complete
Safety Evaluation Prior to Installation of Temporary Modification .. 14
E8.2
(Closed) URI 50-220 5 50-410/96-14-02:
Potential Over-
pressurization Concerns Relative to NRC Generic Letter 96-06 ..
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E8.3
(Closed) URI 50-220/97-12-08:
Impact of Drywell to Wetwell
Bypass on Containment Pressure...... ~..................
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E8.4
(Closed) LER 50-220/98-05:
Unrecognized Violation of TS
Secondary Containment .. ~... ~....
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E8.5
(Closed) LER 50-220/98-06:
Design Deficiency Associated with
CREVS Radiation Monitors ............ ~...............
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E8.6
(Closed) LER 50-410/98-07:
TS 3.0.3 Entry Due to Missed Logic
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System Functional Testing of Loss of Voltage and Degraded
Voltage Channels .. ~.....;....... ~........
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E8.7
(Closed) Part 21 50-220/98-01:
Defective GE SBM-Type
Switches at Unit
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IV. PLANT SUPPORT
R1
Radiological Protection and Chemistry (RPSC) Controls
R1
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Radiological Environmental Monitoring Program Implementation
R1.2
Meteorological Monitoring Program Implementation ........
R1.3
Unit 1 and Unit 2 Tours
R1.4
Unit 2 Refueling Outage .. ~.........
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R1.5
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Quality Assurance
in RPSC Activities.......................
R7.1
Quality Assurance Audit Program
R7.2
Quality Assurance of Analytical Measurements .. ~...... ~;
R7.3
Deviation Event Reports and Self Assessments........
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Status of Security Facilities and Equipment ~..... ~............
S2.1
Tour of the Protected Area Perimeter..... ~....
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S8, Miscellaneous Security and Safeguards
Issues
S8.1
(Closed) URI 50-220 5 50-410/96-06-06:
Fitness-for-Duty
Random Selection Process Software Altered.............
S8.2
Administrative Closure of Escalated Enforcement Items .....
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V. MANAGEMENTMEETINGS........................,................
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Exit Meeting Summary ....................................
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ATTACHMENT
ATTACHMENT1
Partial List of Persons Contacted
Inspection Procedures
Used
Items Opened, Closed, and Updated
List of Acronyms Used
J
C
EXECUTIVESUMMARY
Nine Mile Point Units 1 and 2
50-220/98-05 & 50-41 0/98-05
April 12- May 23, 1998
This NRC inspection report includes reviews of licensee activities in the functional areas of
operations, engineering, maintenance,
and plant support.
The report covers a six-week
period of inspections and reviews by the resident staff and regional specialists in the areas
of environmental monitoring and outage radiation protection.
PLANT OPERATIONS
During performance of a Unit 1 surveillance test, the containment spray raw water inter-tie
check valve did not open with the required torque and the station shift supervisor (SSS)
failed to enter the core spray system TS 3.1.4.d action statement,
as required by the
surveillance test.
The relieving SSS identified the procedural non-compliance and took
prompt and appropriate action to comply with the surveillance procedure.
The failure to
properly implement the surveillance test is a violation of TS 6.8.1.
(VIO 50-220/98-05-01)
While transferring a double blade guide (DBG) from the spent fuel pool to the reactor
vessel, the DBG became disengaged
from the grapple and came to rest in the fuel transfer
canal.
NMPC determined that the root cause was the refueling crew did not properly verify
engagement
of the grapple.
NMPC's root cause investigation was methodical and
thorough, the root cause determination was technically sound, and the corrective actions
adequately addressed
the cause.
MAINTENANCE/SURVEILLANCE
During this inspection period, the NMPC staff self-identified that the TS required service
test of the Unit 2 Division I battery was not completed during the previous two refueling
outages.
NMPC had improperly credited the battery cyclic performance test for satisfying
the requirements of the service test.
NMPC requested
and was granted
a Notice of
Enforcement Discretion (NOED) to avoid the consequential
TS required shutdown.
The
NOED was exited on May 2; 1998 upon the unit achieving Cold Shutdown conditions and
.
the service test was completed satisfactorily on May 7, 1998. Notwithstanding, the failure
to have properly service tested the Division I battery, since April 1995, is a violation of TS 4.8.2.1.d.
(VIO. 50-410/98-05-02)
ENGINEERING
During surveillance testing of the Unit 2 Division II EDG, a fuel leak developed between the
fuel filter and the fuel injectors.
NMPC determined that the leak was caused by vibration
of the fuel supply piping, which caused fretting of the pipe at a pipe support.
Subsequent
licensee investigation identified notable, but less severe, fretting on the Division I EDG fuel
supply piping. The fuel line supports were installed in 1993, but the specific design
change to install a protective grommet.was not adequately incorporated into the final
Jl ~
Executive Summary (cont'd)
design package.
This is a violation of 10CFR50, Appendix B, Criterion III, "Design
Control." (VIO 50-410/98-05-03)
The design and installation of the new ECCS pump suction strainers appeared
adequate to
ensure sufficient net positive suction head for the pumps in the event of a loss of coolant
accident (LOCA).
During a review of Unit 1 operating procedures,
NMPC identified that the normally open
vent valves on the containment spray raw water heat exchangers
violated secondary
containment integrity, in that it provided a potential release path from the reactor building
to the environment.
This licensee identified and corrected violation of secondary
containment integrity requirements was not cited.
During a review of the control room emergency ventilation system initiation.logic, NMPC
determined that the system would not automatically initiate, as required.
Specifically, the
system would not automatically start as a result of a main steam line break or a loss of
coolant accident.
This licensee identified and corrected violation of 10CFR50, Appendix B,
Criterion XI, "Test Control," was not cited.
The inspectors observed that NMPC's follow-up of the Part 21 report concerning GE SBM-
type control switches and their identification of the susceptible switches at Unit 1 was
thorough and an example of an improving questioning attitude by the engineering staff.
PLANT SUPPORT
The licensee effectively maintained and implemented the Radiological Environmental
Monitoring Program in accordance with regulatory requirements.
The licensee performed,a
comprehensive review of an anomalous. indication of Iodine 131 in an environmental milk
sample.
Overall, the licensee effectively maintained meteorological monitoring system operability,
and satisfactorily performed channel calibrations and channel functional tests for the
meteorological instrumentation, with the exception of the wind speed channel.
The failure
to perform the channel calibration of the wind speed channel according to the channel
calibration definition in TS 1.4, in that the accuracy of the entire wind speed chan'nel was
not measured from the sensor to the channel output, constitutes
a violation of Unit 2 TS
3/4.3.7.3.
(VIO 50-410/98-05-06)
Housekeeping was adequate
in that aisles and walkways were clear and free of debris,
radiological boundaries and postings were clear, and access controls to radiologically
controlled areas were effective.
Radiological controls for outage work were well planned and health physics personnel
maintained close oversight of work.
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Executive Summary (cont'd)
Procedure S-RPIP-5.4, "Dose Tracking and Timekeeping," lacked clarity with regard to the
method for determining the available administrative extremity exposure,
and several
examples of inaccurate determinations of available administrative extremity exposure were
identified.
ALARAgoals were effectively used as a tool to aid radiological planning to minimize
radiation exposure.
Numerous ALARAinitiatives including publication of a pre-outage
report, use of cameras,
use of temporary shielding, planned reactor vessel nozzle hydro
washes,
and an attempt to chemically decontaminate the reactor recirculation system
demonstrated
management
support and a commitment to maintaining radiation exposures
The contractor laboratory continued to implement effective QA/QC programs for the REMP,
and continued to provide effective validation of analytical results.
The laboratory
demonstrated
the ability to accommodate
and incorporate difficultmedia and geometries
into the program.
The programs are capable of ensuring independent checks on the
precision and accuracy of the measurements
of radioactive material in environmental
media.
The DER system and the self-assessment
program were effective in their use to identify,
evaluate, and resolve radiological program deficiencies.
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REPORT DETAILS
~ Nine Mile Point Units 1 and 2
50-220/98-05 5 50-410/98-05
April 12- May 23, 1998
SUMMARYOF ACTIVITIES
Niagara Mohawk Power Corporation (NlVIPC) Activities
Unit 1
Nine Mile Point Unit 1 (Unit 1) started the inspection period at full (100%) power.
On April
21, 1998, Unit 1 entered
a 7-day Technical Specification (TS) Limiting Condition of
Operation (LCO) due to the determination that the control room emergency ventilation
system (CREVS) would not automatically initiate as designed
(see Section E8.5 of this
inspection report).
Because the repairs could not be completed before the expiration of the
LCO, Unit 1 was shutdown on April 27.
Following CREVS modifications, the unit was
restarted shortly after the end of the inspection period, and obtained full power on June 1,
1 998.
Unit 2
Nine Mile Point Unit 2 (Unit 2) started the inspection period at 91% power, in a coast-
down condition as they neared the next refueling outage.
On May 2, the unit was
shutdown to start the sixth refueling outage (RFO6). The unit remained shutdown through
the end of the inspection period.
Nuclear Regulatory Commission (NRC) Staff Activities
Ins ection Activities
The NRC resident inspectors conducted inspection activities during normal, ba'ckshift, and
deep backshift hours.
In addition, specialist from Region
I conducted inspections in the
area. of environmental monitoring and outage radiation protection.
The results of the
inspection activities are contained in the applicable sections of this report.
U dated Final Safet
Anal sis Re ort Reviews
While performing the inspections discussed
in this report, the inspectors reviewed the
applicable portions of the Updated Final Safety Analysis Report (UFSAR) related to the
areas inspected.
The inspectors verified that the UFSAR wording was consistent with the
observed plant practices, procedures
and/or parameters.
l
01
Conduct of Operations
01.1
General Comments
71707 '.
OPERATIONS
The resident inspectors conducted frequent reviews of ongoing plant operations to
determine if the units were operated safely and in accordance with licensee
procedures
and regulatory requirements.
The reviews included tours of accessible
and normally inaccessible
areas of both units, verification of engineeied safeguards
features
(ESF) system operability, verification of adequate
control room and shift
staffing, verification that the units were operated
in conformance with technical
specifications, and verification that logs and records accurately identified equipment
status or deficiencies. 'In general, the conduct of operations was professional and
safety-conscious;
specific events and noteworthy observations
are detailed in the
sections below.
01.2
Unit 1 - Failure to Follow Surveillance Test Procedure
a.
Ins ection Sco
e 71707
The inspectors reviewed the circumstances
surrounding the failure of Unit 1 to
perform actions specified by a surveillance test procedure due to unsatisfactory
surveillance test data.
b.
Observations
and Findin s
On April 22, 1998, during performance of NMPC surveillance test Procedure
N1-ST-
Q28, "Containment Spray Raw Water Inter Tie Check Valve'Quarterly Operability
Test," check valve 93-64 (containment spray raw water sub-loop 122 to core spray
loop 12 testable check valve) failed to open with the required torque.
The.day-shift
station shift supervisor (SSS) was notified of the valve failure at 12:07 p.m.; he
entered Unit 1 TS 3.3.7.b, with a 15-day LCO for an inoperable containment spray
loop and DER 1-98-0960 was initiated to address the concern.
At 8:43 p.m., the night-shift SSS noted that actions contained in N1-ST-Q28 had
not been completed.
Note
1 after Step 10.1.1 (Operations Review of the
Acceptance Criteria) stated that if check valve 93-64 failed, then loop 12 was to be
considered inoperable; subsequently,
TS LCO 3.1.4.d needed to be entered, which
required a shutdown be initiated within 1 hour1.157407e-5 days <br />2.777778e-4 hours <br />1.653439e-6 weeks <br />3.805e-7 months <br /> and be in a cold shutdown condition
within the next 10 hours1.157407e-4 days <br />0.00278 hours <br />1.653439e-5 weeks <br />3.805e-6 months <br />.
Note 2 stated that the LCO could be exited if one of the
blocking valves was closed.
The SSS directed both blocking valves shut, and
1 Topical headings such as 01, M8, etc., are used in accordance with the NRC standardized reactor inspection report outline.
Individual reports are not expected to address
all outline topics.
The NRC inspection manual procedure or temporary instruction
(Tl) that was used as inspection guidance is listed for each applicable report section.
4
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exited LCO 3.1.4.d at 9:20 p.m. The failure to adhere to procedure N1-ST-Q28 is a
violation of the Unit 1 TS 6.8.1.
(VIO 50-220/98-05-01)
The inspectors discussed the check valve failure with the system engineer, who
stated that check valve 93-64 appeared to have been hydraulically locked.
The
system was vented and the valve retested satisfactorily.
The system engineer
stated that the mechanism for the hydraulic locking would be investigated further.
C.
Conclusion
During performance of a Unit 1 surveillance test, the containment spray raw water
inter-tie check valve did not open with the required torque and the station shift
supervisor (SSS) failed to enter the core spray system TS 3.1.4.d action statement,
as required by the surveillance test.
The relieving SSS identified the procedural non-
compliance and took prompt and appropriate action to comply with the surveillance
procedure.
The failure to properly implement the surveillance test is a violation of
(VIO 50-220/98-05-01)
01.3
Conduct of Unit 2 Core Off-load 0 erations
60710
The inspectors observed licensee and contractor, General Electric (GE), conduct of
operations during Unit 2 core off-load. The inspectors observed the evolution from
the control room, and the refuel floor, during both normal and back shift hours.
The
inspectors also reviewed applicable procedures
and TS to verify licensee
compliance.
The inspectors observed operations staff and GE personnel perform fuel movement
from the refuel bridge and considered the evolutions well controlled.
personnel exhibited good formal communication, and completed the evolution in
accordance with procedures.
'Before RFO6, NMPC replaced the triangular refueling mast with a heavier round
mast that included an installed camera and monitoring system.
The modification
required a TS amendment, which was approved by the NRC, via letter dated April
16, 1998.
During the off-load evolutions, no concerns were noted with'the
operation of the new refueling mast.
Moreover, the inspectors noted that the
installed camera system greatly enhanced the operators'bility to verify fuel bundle
serial numbers before grapple engagement.
01.4
Dro
ed Double Blade Guide Durin
Unit 2 Off-load 0 eration
Ins ection Sco
e 60710 93702
The inspectors reviewed the circumstances
surrounding the dropped double blade
guide (DBG) during the Unit 2 core off-load. A DBG is used to provide lateral
support for fully inserted control rods during off-load conditions; wHen fuel is in the
reactor vessel, control rods are supported laterally by the surrounding fuel bundles.
The inspectors assessed
the licensee's
response to the event, including the
4
T
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immediate actions, root cause determination, and corrective actions.
In addition,
the inspectors visually observed the location of the DBG as it rested in the transfer
canal, monitored a Station Operating Review Committee (SORC) meeting associated
with the event, reviewed the applicable procedure and DER, and discussed
related
issues with the Senior Reactor Operator (SRO) on the refuel bridge at the time of
the event, members of the root cause analysis team, and the Unit 2 Plant Manager.
Observations
and Findin s
On May 19, 1998, while transferring a DBG from the spent fuel pool (SFP) to the
reactor vessel, the DBG became disengaged
from the grapple and fell onto the fuel
transfer canal.
The refueling bridge SRO immediately stopped all fuel handling
activities and informed the control room of the situation.
Management and
technical support staff assisted
in the evaluation of the situation.
An underwater
video camera was used to view the grapple and the DBG bail (handle)
~ The grapple
was closed and the,"engaged" light on the refuel platform control panel was
illuminated. The DBG bail handle appeared to be intact with no indication of failure.
The licensee issued
a DER to record the event and a root cause analysis team was
formed.
Upon being informed of the event, the inspectors performed a visual
inspection of the refuel floor, the SFP and reactor cavity, and considered the DBG to
be in a stable condition.
NMPC developed
a plan and retrieved the DBG. They
inspected it for damage,
and returned it to its previous location in the SFP.
During NMPC's root cause investigation, the grapple and the DBG handle were
measured,
inspected
and tested to determine how the DBG may have dropped from
the grapple.
GE, the manufacturer of the grapple, was contacted for assistance.
By evaluating the dimensions of the grapple and attempting to duplicate the event,
NMPC determined the following as the most probable scenario:
When the grapple
was brought into position over the DBG, it was slightly mis-oriented such that the
DBG bail handle wedged diagonally between the bail handle channel on one side of
the grapple shroud and the corner of the shroud on the opposite side.
In this
position, the grapple was ready to engage the bail handle; however, the mast was
approximately one-inch higher then normal for DBG engagement.
When the signal
was given for the grapple to engage the bail, the middle hook of the grapple
traveled to the normal engaged position, but the outside hook came to rest against
the bail handle.
In this condition, the "engaged" light would not have been
illuminated since the necessary
contacts within the circuitry would not be closed.
The DBG was lifted to the "full-up"position and moved to the fuel transfer canal.
To transverse through the fuel transfer canal, the bridge operator rotated the mast
90'o align the DBG with the transfer canal.
As the bridge accelerated,
the DBG
slipped from the single grapple hook; at this time; the "grapple engaged" light
illuminated since the grapple hooks would have closed after the DBG fell.
The licensee tested this scenario several times with confirmatory results.
All details
noted during the tests corresponded to those described by the refueling operators
following the event with one exception.
During the post event interviews, the fuel
handler and spotter stated that the "engaged" light was lit before the DBG was
lifted. During the tests, the "engaged" light was never received before the blade
4
e
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.5
guide lift. Based on the above, the licensee determined that the root cause
was'hat
the refueling crew did not properly verify grapple alignment, resulting in a
partial engagement of the DBG.
Prior to continuing core off-load, NMPC implemented several corrective and
preventive actions, as documented
in DER 2-98-1415.
The actions included:
(1)
adding a column to the fuel move sheets to document the receipt of the "grapple
engaged" light prior to lifting fuel assemblies
or blade guides, and (2) training of the
refueling crews on the issues associated with the event.
Based on an analysis from
GE, NMPC further concluded that physical design differences between the blade
guide bail handle and the fuel assembly bail handle would prevent a similar
occurrence with a fuel assemble.
NMPC completed core off-load on May 23,
without further incident.
Based on the inspectors review, NMPC's root cause investigation appeared
methodical and thorough, the root cause determination was technically sound, and
the corrective actions adequately addressed
the cause.
C.
Conclusion
While transferring a double blade guide (DBG) from the spent fuel pool to the
reactor vessel, the DBG became disengaged from the grapple and came to rest in
the.fuel transfer canal.
NMPC determined that the root cause was the refueling
crew did not properly verify engagement
of the grapple.
NMPC's root cause
investigation was methodical and thorough, the root cause determination was
technically sound, and the corrective actions adequately addressed
the cause.
08
Miscellaneous Operations Issues
08.1
Closed
LER 50-410 98-05: Reactor Water Cleanu
Isolation on Hi h Differential
Flow Caused
b
Relief Valve Liftin
92700
On March 17, 1998, while placing a reactor water cleanup (RWCU) system filter
demineralizer in service, Unit 2 experienced
an automatic isolation of the 'system
due to high differential flow. The operators verified proper system response,
implemented the TS action statements,
and wrote a DER to investigate the cause of
the system isolation.
Subsequently,
NMPC identified that the filter demineralizer
relief valve lifted, which caused the high differential flow and resulted in the system
isolation.
The relief valve was disassembled
and NMPC determined that the valve
disk seating surface was degraded.
A new valve was installed.
The day of the
event, the inspectors discussed the RWCU system isolation with the Unit 2 licensed
operators,
and verified the appropriate implementation of TS.
During this inspection period, the inspectors discussed
the root cause determination
with the system engineer and observed the SORC's review of the associated
DER
and Licensee Event Report (LER) 98-05.
No concerns were identified. The
inspectors verified that the LER was completed in accordance with the requirements
of 10CFR50.73.
This LER is"closed.
4t
i
Closed
LER 50-410 98-06:
En ineered Safet
Feature Actuations Due to Partial
Loss of Offsite Power 92700
The technical issues associated with this LER were reviewed and documented
in
Section 01.2 of inspection report (IR) 50-410/98-02.
However, the LER provided
additional information regarding two equipment performance abnormalities that
occurred during the loss of Line 5, one of the two 115KV sources of offsite power.
Specifically, the Division II hydrogen/oxygen (H,O,) sample pump and the Division II
cable spreading area unit cooler both tripped during the transient and had to be
manually restarted.
These components were not expected to trip since Division II
was being powered by Line 6, the other 115KV offsite power source.
evaluated the circuits associated with these components
and verified that there was
no inter-tie with Division I or III power.
However, they did identify a loose
connection within the control circuitry for each component.
Also, the loss of Line 5
caused
a transfer of load to Line 6, resulting in a momentary drop in Line 6 voltage.
NMPC determined that the loose connections, combined with the voltage drop on
Line 6, was sufficient to cause these components to trip. Although loose
connections existed, NMPC concluded that the equipment was able to perform the
intended design function. The inspectors considered NMPC's conclusion to be
technically sound.
The inspectors verified that the LER was completed in accordance with the
requirements of 10CFR50.73.
This LER is closed.
r
Closed
LER 50-410 98-08: HPCS Out of Service with One Division of RHS in
Su
ression Pool Coolin
Ins ection Sco
e 92700
The inspectors reviewed the LER, the UFSAR, related DERs, and the NMPC design
specification related to the emergency core cooling system (ECCS).
In addition, the
inspectors discussed the issue with the system engineer and a licensing engineer,
and observed
a Unit 2 SORC meeting regarding the issue.
The inspectors verified
the completion of the LER in accordance with 10CFR50.73.
Observations
Findin s and Conclusions
In March 1998, as a result of operating experience reviews, NMPC initiated a DER
to investigate
a concern regarding the operability of the residual heat removal
system (RHS) while operating in the suppression
pool cooling mode.
Specifically, as
originally designed, the closing time (120 seconds) of the suppression
pool cooling
valve was slower than the opening time (65 seconds) of the low pressure coolant
injection (LPCI) mode injection valve. Therefore, during suppression
pool cooling,
full LPCI flow. would not be available until the suppression
pool cooling valve was
completely closed.
As a result, during suppression
pool cooling, the RHS division
would be inoperable for the LPCI mode.
NMPC reviewed operational history and
determined that, based on this scenario, TS requirements had not been exceeded.
Afterwards, NMPC determined that during RHS full flow test, the system would also
J
4
be inoperable, because the test configuration uses the suppression
pool cooling
valve.
Licensee review identified that, on January 25, 1996, Unit 2 had operated for
twelve minutes with the high pressure
core spray (HPCS) system out-of-service at
the same time that Division II RHS was in the full flow test configuration.
In this
configuration, TS 3.0.3 was applicable since no specific TS requirement existed to
cover this condition.
Based on the information provided in the LER, and a review of
the applicable TS, the inspectors concluded that no TS violation had occurred,
because the twelve minutes that HPCS and Division II RHS were concurrently
inoperable was within the one hour LCO allowed by TS 3.0.3.
However, the failure
to have adequately reviewed the suitability of the suppression
pool cooling/full flow
test valve closing time with respect to the LPCI functions of RHS constitutes
a
.
violation of minor significance and is not subject to formal enforcement action.
The inspectors verified that the LER was completed in accordance with the
requirements of 10CFR50.73.
This LER is closed.
II. MAINTENANCE
M1
Conduct of Maintenance
M1 ~ 1
General Comments
61726 62707
The resident inspectors periodically observed plant maintenance
activities and the
performance of various surveillance tests.
As part of the observations, the
inspectors evaluated the activities with respect to the requirements of the
Maintenance
Rule, as detailed in 10CFR50.65.'n general, maintenance
and
surveillance activities were conducted professionally, with the work orders (WOs)
and necessary
procedures
in use at the work site, and with the appropriate focus on
safety.
Specific activities and noteworthy observations
are detailed in the
inspection report.
The inspectors reviewed procedures and,observed
all or portions
of the following maintenance/surveillance
activities:
N1-ESP-RPS-331
N1-IPM-036-010
N1-IPM-036-040
N1-ISP-036-1 03
N1-ISP-036-1 04,
Reactor Protection System Motor-Generator Set
Instrument Channel Test Excluding Output Contractors
Anticipated Transient Without Scram /Alternate Rod
Injection Instrument Calibration
Yarway Reactor Level Local Indicator Calibration
Hi/Lo Rx Water Instrument Trip Channel Calibration
Low-Low Rx Water Level Instrument Trip Channel
Calibration.
P
Surveillance activities are included under "Maintenance.
For example,
a section involving surveillance observations might
be included as a separate sub-topic under M1, "Conduct of Maintenance."
f
e
~
N1-ST-V3
N2-ESP-BYS-R681
N2-FHP-1 3.1
N2-MSP-EGS-R02
N2-OSP-EGS-R04
N2-PM-S001
WO 97-12419-00
WO 97-16778-01
WO 97-16778-03
WO 97-16778-12
'WO 98-1192-00
WO 98-21 59/60
WO 98-2243-02
WO 98-2211-00
WO 98-2211-02
WO 98-2211-04
WO 98-2327-04
Rod Worth Minimizer Operability Test APRM/IRM
Overlap Verification
Div I/II/IIIBattery Service Test
Complete Core Off-load
Diesel Generator Inspection Division 3 (EGS "EG2)
Operating Cycling Diesel Generator Simulated Loss of
Offsite Power with ECCS Division I 5, II
Refueling Platform and Grapple Inspection
N2-MSP-EGS-R002- Diesel Generator Inspection - Div.
III (18 month, 6 5 12 year Requirements)
Pre-staging Activities to Support ECCS Suction Strainer
Modification N2-97-067
Remove Existing ECCS Strainer 2CLS "STR1 and
Replace with New Strainer
Transport of New ECCS Suction Strainers into the
Suppression
Pool and Removal of Old ECCS Suction
Strain ers
Work Order for N1-ESP-RPS-331
Input New Set Points for Control Room Ventilation
Radiation Monitor ¹11/12
Relocate Radiation Detector per DDC 1M00571
Fabricate
5, Install Plate for Controls per DDC 1F00460
Make Wire Changes to Provide Manual Control to TCV-
210.1-56 per 1F0460 Latest Revision
Support Ears to Mount Valve Position Indicator, Plate
Broken Off
Perform MFT for CRAG Mod.(N1-MFT-053)
.
M8
Miscellaneous Maintenance Issues
M8.1
Closed
URI 50-220 96-01-03: Inade
uate Testin
of Unit 1 Control Room
=Annunciators
a.
Ins ection Sco
e 92902
The inspectors reviewed NMPC's response to a lack of preventive maintenance
and
calibration of annunciator inputs at Unit 1. The inspectors discussed the disposition
of the associated
DER with Unit 1 management.
b,
Observations
Findin s and Conclusion
.
The inspectors reviewed the disposition of DER 1-96-0148regarding
the
January 20, 1996 trip of the Unit 1 ¹11 reactor feed pump due to a relay failure.
The DER addressed
the failure of the Agastat relay and associated
corrective
actions.
However, the unresolved item was initiated due to the inspectors'oncern
that the associated
control room annunciator did not alarm, as expected,
and to
assess
the adequacy of periodic control room annunciator testing.
t
i
0
Discussions with the Unit 1 Technical Support Manager and the General Supervisor
of Operations revealed that all annunciator inputs are either tested or determined to
be not necessary for safe operation.
After a licensee review of this concern, the
reactor feed pump trip annunciator and a few additional annunciators were found to
have been improperly categorized
as not necessary for safe operation.
The
inspectors determined that this oversight of annunciator testing constituted
a
violation of minor safety significance and is not subject to formal enforcement
action.
M8.2
Closed
URI 50-410 96-10-01: Post-Maintenance
Testin
of the Unit 2 Main
Steam Line Radiation Monitors
92902
During a review of the post-maintenance
testing (PMT) of the Unit 2 main steam
line (MSL) radiation monitor, the inspectors noted that the TS required trip signals
were cleared to support the PMT. The inspectors questioned the removal of the trip
signals while the channel was still inoperable and the LCO action statement was still
effective.
The licensee stated that the trip signal needed to be cleared to perform
the PMT surveillance before the channel could be declared operable.
Notwithstanding good justification, the removal of the LCO required trips prior to
declaring the MSL radiation monitor operable appeared to be in conflict with Unit 2
NMPC challenged this interpretation of TS 3.3.1 and submitted a letter.to
the NRC, dated October 21, 1996, requesting
a clarification of "... a longstanding
[industry] practice that permitted the conduct of TS surveillance testing needed to
demonstrate that previously inoperable equipment had been restored to an operable
condition."
On November 21, 1996, the NRC responded with the following: "... It is not the
intent of TS 3.0.2 to preclude the return to service of a component that has been
replaced or repaired when it can reasonably
be considered operable except for the
'ompletion of.surveillance testing to confirm its operability.
The NRC staff has
addressed
this existing ambiguity in TS 3.0.2 by adding TS 3.0.5 to the Standard
Technical Specifications for BWR/4, Revision 1. TS 3.0.5 states "... equipment
removed fiom service or declared inoperable to comply with ACTIONS may be
returned to service under administrative control solely to perform testing required to
demonstrate
its OPERABILITYor the OPERABILITYof other equipment
. ~."
Based upon the above, NMPC's post-maintenance
testing practices are acceptable
and there is no violation of regulatory requirements.
This unresolved item is closed.
M8.3
Closed
VIO 50-410 96-10-03: Procedure
Chan
es Not in Accordance with TS
Re uirements
92902
In August 1996, during repairs to the Unit 2 control building chillers, a procedure
change evaluation (PCE) was processed to change the service water low flow set
point. However, the PCE was processed
as an editorial change and did not receive
the approval of a senior reactor operator, as required by the Unit 2 TS 6.8.3. This
was documented
on DER 2-96-3284.
P
0
10
The inspectors reviewed the DER disposition and NMPC's response to the Notice of
Violation. Corrective actions included revising the common site procedure which
controls PCEs (NIP-PRO-04) to clarify and limitwhat may be considered
an editorial
change to a procedure.
The inspectors have identified no further examples of
improperly processed
PCEs.
This violation is closed.
M8.4
Closed
VIO 50-410 97-02-02: Missed Unit 2 HPCS Actuation Instrumentation TS
Surveillance Test 92702
In March 1997, NMPC identified that their test procedures failed to satisfy the TS
surveillance requirements
(TSSR) for response time testing of the HPCS actuation
instrumentation.
NMPC's letter, dated June 16, 1997, provided the root cause and
corrective actions for this violation; much of the same information was also
contained in LER 50-410/97-01.
The inspectors'eview of the immediate corrective
actions was detailed in IR 50-410/97-02 and the inspectors'eview of the
associated
LER was documented
in IR 50-410/97-04.
The inspector determined
that the licensee reviewed other ECCS response time tests with no additional
deficiencies identified. With respect to actions to prevent recurrence,
credited improvements to their procedure review process
as barriers to prevent
recurrence.
The inspectors re'viewed the enhanced
administrative control
procedures
and identified no concerns.
This violation is closed.
M8.5
Closed
LER 50-410 98-09: Missed Batter
TSSR Due to Ina
ro riate
aO
Ins ection Sco
e 61726 92700
The inspectors reviewed the LER, DER, and applicable TSs, surveillance test
procedures
and test results, and discussed this issue with responsible individuals.
In addition, discussions were held with NRC management
and technical staff
members from the Region
I Office and the Office of Nuclear Reactor Regulations
(NRR) with regard to enforcement discretion.
Also, the inspectors verified the
completion of the LER in accordance with 10CFR50.73.
b.
Observations
and Findin s
On April 17, 1998, NMPC determined that TSSR 4.8.2.1.d for the Division I 125
volt battery had not been met for Unit 2 from April 5, 1995, to the present.
Specifically, during RFO4 and RFO5, credit was inappropriately taken for the battery
performance test in lieu of the battery service test.
Upon identification of the
missed surveillance, the Unit 2 SSS declared the Division I battery inoperable.
Before initiating the TS required plant shutdown, NMPC notified the NRC and
requested
enforcement discretion to delay the testing of the battery until RFO6,
scheduled to begin May 2, 1998.
The NRC verbally granted enforcement discretion
from the TS requirements until the next Unit 2 entry into Cold Shutdown, but not
later than May 3, 1998. This discretion allowed NMPC to avoid an unnecessary
'lant shutdown.
The enforcement
discretion was granted provided that the
Division II and III batteries remained'operable
and the Division I battery cell-to-cell
11
resistance
check were performed weekly.
On April 21, 1998, the written Notice of
Enforcement Discretion (NOED) was docketed.
Notwithstanding, the failure to
complete the required Division I battery service test, since April 1995, is a violation
of TS 4.8.2.1.d.
(VIO 50-410/98-05-02)
On May 2, 1998, Unit 2 shutdown for RFO6 and the NOED was exited upon the
unit achieving the Cold Shutdown condition.
On May 7, NMPC successfully
completed the service test on the Division I battery.
The inspectors reviewed the
test procedure and results, and identified no concerns.
The inspectors verified that the LER was completed in accordance with the
requirements of 10CFR50.73.
This LER is closed.
c;
Conclusion
During this inspection period, the NMPC staff self-identified that the TS required
service test of the Unit 2 Division I battery was not completed during the previous
two refueling outages.
NMPC had,improperly credited the battery cyclic
performance test for satisfying the requirements of the service test.
requested
and was granted a Notice of Enforcement Discretion (NOED) to avoid the
consequential
TS required shutdown.
The NOED was exited on May 2, 1998 upon
the unit achieving Cold Shutdown conditions and the service test was completed
satisfactorily on May 7, 1998.
Notwithstanding, the failure to have properly service
tested the Division I battery, since April 1995, is a violation of TS 4.8.2.1.d.
(VIO 50-41 0/98-05-02)
III. ENGINEERING
E1
Conduct of Engineering
E1.1
General Comments
37551
The resident inspectors frequently reviewed design and system engineering
activities, including justifications for operability determinations,
and the support by
the engineering organizations to plant activities.
E1.2
Unit 2 Emer enc
Diesel Generator Fuel Line Leak
a.
Ins ection Sco
e 37551
During a Unit 2 surveillance test of the Division II emergency diesel generator (EDG),
a fuel leak developed in the pipe between the fuel filters and the fuel injectors.
The
inspectors assessed
NMPC's actions to address
and evaluate the leak. The
assessment
included a visual inspection of the damaged fuel line and the
susceptible location on the other Unit 2 EDGs, and a review of associated
DERs,
SSS's logs, plant modifications, UFSAR and TS sections,
and immediate and long-
k
12
term corrective actions.
The inspectors discussed
issues related to the event with
the Unit 2 Plant Manager and members of the Unit 2 system engineering staff.
Observations
and Findin s
On April 14, 1998, during a surveillance test of the Division II EDG, a fuel leak
dev'eloped in the fuel line pipe between the fuel filters and the fuel injectors.
The
operators immediately stopped and shutdown the EDG. The SSS declared the EDG
inoperable, the appropriate TS LCO was entered; and a DER was initiated to record
the event.
Upon investigation, NMPC concluded that vibration of the fuel line pipe
caused fretting of the piping at the location of a pipe support.
NMPC generated
a
work order to replace the pipe and, after repairs were completed, declared the EDG
operable on April 15.
As required by TS, NMPC evaluated the other EDGs for susceptibility to the same
failure mechanism.
The Division III EDG is of a different design and is not
susceptible.
However, NMPC identified notable degradation of the fuel line at the
same location on the Division I EDG. After close examination, NMPC concluded
that the degradation was not significant enough to impact operability.
The
inspectors discussed the basis for the operability determination with the SSS and
the system engineer, and considered it adequate.
I
On April 18 NMPC replaced the Division I EDG degraded fuel line pipe.
Besides
replacing the pipe, NMPC evaluated and incorporated
a design change to install a
rubber grommet between the pipe and the support to prevent recurrence.
Subsequently,
a similar design change was completed for the Division II EDG pipe
support.
Following the event, NMPC evaluated the consequence
of the Division II EDG fuel
line leak and concluded that based on the size of the leak and the available fuel
within the storage tank, the EDG was capable of operating at rated load for seven
days, as designed.
The resident inspectors and region-based
specialists reviewed
the evaluation and determined that the licensee's conclusion was acceptable.
NMPC reviewed the history of these fuel lines and revealed that a 1993 design
change added the pipe supports to correct previous fuel line leaks.
Further
investigation revealed that the design package included a rubber grommet at the
pipe support, to compensate for system vibration. However, the requirement to
install the protective grommet was not adequately incorporated into the final design
package.
The failure to translate
a specific design change to correct an identified
design deficiency into the design package
is contrary to 10CFR50, Appendix B,
Criterion III, "Design Control," and is a violation.
(VIO 50-410/98-05-03)
Conclusion
'
During surveillance testing of the Unit 2 Division II EDG, a fuel leak developed
between the fuel filter and the fuel injectors.
NMPC determined'that the leak was
caused by vibration of the fuel supply piping, which caused fretting of the pipe at a
r
13
pipe support.
Subsequent
licensee investigation identified notable, but less severe,
fretting on the Division I EDG fuel supply piping. The fuel line supports were
installed in 1993, but the specific design change to install a protective grommet
was not adequately incorporated into the final design package.
This is a violation of
10CFR50, Appendix B, Criterion III, "Design Control." (VIO 50-410/98-05-03)
E3
Engineering Procedures
and Documentation
E3.1
Unit 2 ECCS Suction Strainer Modification
a.
Ins ection Sco
e 37551
In response to NRC Bulletin 96-03, NMPC installed new ECCS suction strainers in
the Unit 2 suppression
pool. The inspectors reviewed the engineering design
documents, the associated
work orders, and observed the installation of the new
strainers.
b.
Observations
Findin s
and Conclusion
In May 1996, the NRC issued Bulletin 96-03 ("Potential Plugging of Emergency Core
Cooling Suction Strainers by Debris in Boiling Water Reactors" ) which addressed
concerns that the strainers would become plugged by debris during a loss of coolant
accident.
The Bulletin proposed several options, NMPC chose the installation of
large capacity passive strainers at Unit 2; in that the existing strainers could not
accommodate the projected debris loading.
NMPC designed and installed new
suction strainers for the residual heat removal, low pressure
core spray, and high
pressure core spray systems to satisfy the system pump net positive suction head
requirements.
The new strainers are of a stacked-disk design and constructed of
type 304 stainless steel.
All work was accomplished
in accordance with the
respective TSs for the associated
safety systems.
In addition to the work orders (listed in Section M1.1) for the removal and
installation of the strainers, the inspectors reviewed the below listed documents
related to the strainer modification. The inspectors identified no concerns or
unreviewed safety questions,
and the proposed changes to the UFSAR appeared
appropriate.
NMP2-41 5M
DDC 2M11330
DCN N2-97-067
DDC 2S11055A
DDC 2S11067
Engineering Specification for Bidding Purposes for
Replacement of ECCS Suction Strainers
Design Document Change to NMP2-415M after Award
Design Change Notification for the'Modifications
Required to Provide Access for the ECCS Strainer
Replacement - Structural, Mechanical, Electrical, and
Removal of South Suppression
Pool Hatch Wall &
Mezzanine for ECCS Strainer Replacement
Field Tolerances for Installation of ECCS Strainers
t
,14
DDC 2M11294
SE 98-033
LDCR 2-97-150
Technical Justification and Installation of ECCS
Strainers
Safety Evaluation for ECCS Suction Strainer
Replacement
Licensing Document Change Request for UFSAR
Changes due to ECCS Suction Strainer Replacement
The design and installation of the new ECCS pump suction strainers appeared
adequate to ensure sufficient net positive suction head for the pumps in the event
of a loss of coolant accident (LOCA).
E8
.
Miscellaneous Engineering Issues
E8.1
Closed
VIO 50-220 5 50-410 96-01-05: Failure to Com lete Safet
Evaluation
Prior to Installation of Tem orar
Modification 92903
E8.2
On January 31, 1996, the inspectors identified the installation of an emergency
temporary modification on the Unit 2 circulating water system prior to the
completion of the required 10CFR50.59 safety evaluation.
Furthermore, NMPC
Procedure GAP-DES-03, "Control of Temporary Modifications," Revision 4,
permitted the installation of emergency temporary modifications.
NMPC letter,
dated May 22, 1996, documented the root. cause and corrective actions for this
violation. The inspectors'eview of the immediate corrective actions was
documented
IR 50-220 &. 50-410/96-01. With respect to actions to prevent
recurrence,
NMPC removed the provision for emergency temporary modification
from the temporary modifications procedure.
Based on the inspectors'eview of
the licensee's corrective and preventive actions, and observation that there have
been no subsequent
installations of a temporary modification prior to the completion
of the associated
safety evaluation, this violation is closed.
Closed
URI 50-220 5 50-410 96-14-02: Potential Over- ressurization Concerns
Relative to NRC Generic Letter 96-06 92903
During the evaluation of NRC Generic Letter (GL) 96-06, "Assurance of Equipment
Operability and Containment Integrity during Design-Basis Accident Conditions,"
NMPC identified some system piping penetrating the drywell that could potentially
be over-pressurized
during a design basis LOCA. Subsequent
NMPC examination of
each penetration,
in accordance with the guidance provided in GL 96-06, concluded
that the systems remained operable.
An unresolved item was assigned to track the
licensee's resolution of this generic issue and to assess
whether this condition was
potentially outside the design bases of the plants.
Subsequent
discussions between the NRC Region
I Office and NRR concluded that
thermal over-pressurization
is not necessarily
a condition outside the design bases
of the plant.
NRC-staff follow-up of each licensee's actions to address
issues will be assessed
via a future inspection activity. This unresolved item is
closed.
I
15
j
E8.3
Closed
URI 50-220 97-12-08: Im act of Dr well to Wetwell B
ass on
Containment Pressure
90712 92903
On October 12, 1997, GE issued
a 10CFR21 (Part 21) notification regarding the
'ossible reduction in the pressure
suppression capability of the torus due to bypass
leakage between the drywell and the torus.
During review of the Part 21
notification for Unit 1, NMPC determined that, although the specific issue described
in the Part 21 was not a concern at Unit 1, other conditions may challenge the
pressure suppression
capability of the torus.
Particularly, during drywell and torus
inerting, deinerting, and primary containment pressure maintenance
evolutions, the
drywell and torus vent valves were usually open concurrently, establishing
a
drywell-to-torus bypass pathway.
Upon identification of this vulnerability, NMPC
issued
a procedure change to prohibit concurrent opening of both the'rywell and
torus vent and purge valves during primary containment venting, filling, and make-
up evolutions.
NMPC issued
LER 50-220/97-15to document this condition.
However, at that
time, NMPC had yet to complete their analysis to determine whether the
containment design pressure would be exceeded
should a LOCA have occurred
while the drywell-to-torus valves were open.
The inspectors'eview of NMPC's
evaluation of the Part 21, and the LER were provided in NRC IR 50-220/97-12.
As
documented
in the IR, the issue was unresolved pending the completion of NMPC's
analysis.
Subsequently,
NMPC completed their analysis and determined that the containment
post-accident pressure, with the bypass pathway, would not have exceeded
maximum design pressure.
Based on this analysis, NMPC retracted
LER 50-220/97-
15 via letter, dated May 1, 1998.
This unresolved item is closed.
E8.4
Closed
LER 50-220 98-05: Unreco
nized Violation of TS Secondar
Containment
a 0
Ins ection Sco
e
92700
The inspectors reviewed NMPC's analysis and corrective actions associated with
the discovery of a breach of Unit 1 secondary containment integrity due to normally
open vents on the containment spray raw water heat exchanger.
b.
Observations
and Findin s
In April 1998, with Unit 1 at full power, NMPC discovered
a breach of secondary
containment.
Specifically, the containment spray raw water (CSRW) heat
exchanger vents were normally open, in accordance with the operating procedure
(N1-OP-14, "Containment Spray" ). The open vents provided a potential
unmonitored release path from the secondary containment (reactor building)
atmosphere,
via the reactor building drain system, through the open CSRW vents,
to the service water system, and to the environment via the service water discharge
to Lake Ontario.
Unit 1 TS, Section 3.4.0, requires reactor building integrity be
maintained during power operation; since the definition of reactor building integrity
16
was not satisfied,
a reactor'hutdown was initiated in accordance with TS 3.0.1.
The procedure was revised, the vent valves were closed, and the shutdown was
terminated at 94% power.
DER 1-98-0903 was written, and the appropriate NRC
notifications were made as required by 10CFR50.72.
The inspectors determined that the original design for the containment spray system
was to operate with the vents open to maximize heat exchanger performance.
In
1986, the vents were closed following the replacement of the heat exchangers.
In
1991, DER 1-91-Q-1417 was written to address concerns associated with the
vents being closed and the effect of non-condensible
gas build-up in the heat
exchangers.
The DER disposition stated that testing 'of the containment spray heat
exchangers
showed that the system would perform its design basis function with
the vents closed.
In addition, the DER noted that the Tube Exchanger
Manufacturers Association (TEMA) recommends that the heat exchanger
be
operated with the vents open.
Therefore, in 1992, a plant change request was
processed to operate with the vents valves open, which would maximize system
performance.
In response to the containment concern and in support of the
decision to close the vent valves, NMPC performed an Operability Determination
and a 10CFR50.59 Applicability Review.
The inspectors discussed this issue with the responsible staff. members and unit-
management,
reviewed the associated
documentation,
and considered the actions
taken and decisions made by'NMPC to have been appropriate.
The LER identified
the cause of the event as inadequate
design analysis, in that, the personnel involved
did not consider the interaction between the open vents and secondary containment
integrity. The analysis of the event revealed that surveillance tests conducted in
1996 and 1997 showed that the reactor building emergency ventilation system
(RBEVS) was able to maintain a negative pressure relative to the environment.
NMPC concluded that operation with the vent valves open would not affect the
ability of the RBEVS to maintain negative pressure
in the event of a design basis
accident.
Notwithstanding', plant operation with secondary containment integrity not properly
established
is a violation of the Unit 1 TS, Section 3.4.0.
However, this non-
repetitive, licensee identified and corrected violation is being treated as a Non-Cited
Violation, consistent with Section VII.B.1 of the NRC Enforcement Policy.
(NCV 50-220/98-05-04)
The inspectors verified that the LER was completed in accordance with the
requirements of 10CFR50.73.
This LER is closed.
Conclusion
During a review of Unit 1 operating procedures,
NMPC identified that the normally
open vent valves on the containment spray raw water heat exchangers
violated
secondary containment integrity, in that it provided a potential release path from the
reactor building to the environment.
This licensee identified and corrected violation
of secondary containment integrity requirements was not cited.
ass
17
Closed
LER 50-220 98-06: Desi
n Deficienc
Associated with CREVS Radiation
Monitors
Ins ection Sco
e 37551
90712
NMPC identified that the radiation monitors for the Unit 1 control room emergency
ventilation system (CREVS) would not have automatically initiated the system in the
event of a main steam line break (MSLB). The unit was shutdown because
repairs
were not able to be completed within the time allowed by the TSs.
The inspectors discussed the issue with various engineering personnel,
and Unit 1
management.
In addition, they monitored portions of the reactor shutdown and the
system modifications.
The inspectors reviewed the DERs, the associated
Safety
Evaluation, implementation of the TS amendment,
and the modification functional
test; the inspectors also performed an in-office review of the LER.
b.
Observations
and Findin s
On April 21, 1998, NMPC identified that the Unit 1 CREVS would not have
automatically initiated, as designed, following a MSLB. The SSS appropriately
entered TS LCO 3.4.5.e, which allowed 7 days to restore the system to an operable
status or required the reactor be shutdown.
NMPC identified that the trip settings
for the radiation monitors installed on the intake of the CREVS were set too high.
Unable to adjust the radiation monitors to properly initiate CREVS for a loss of
coolant accident (LOCA), NMPC initiated a plant shutdown on April 28, which was
completed on April 29.
The inspectors determined that the radiation set point was less than or equal to 800
counts per minute (~800 cpm); this was below the Unit 1 TS required set point of
1000 cpm.
NMPC determined that the set point for MSLB was 6210 cpm, but the
existing monitors'could not be set low enough to detect LOCA conditions.
To
'ensure that the CREVS would initiate for both a MSLB and a LOCA, NMPC proposed
a TS amendment to change the CREVS automatic initiation signal from high
radiation to signals from the reactor protection system for MSLB (main steam line
high flow or main steam line tunnel high temperature)
and LOCA (high drywell
pressure
or low-low reactor pressure vessel water level).
In addition, the set point
for the radiation monitors was adjusted to ~193 cpm.
The NRC approved this TS
amendment on May 23, 1998.
NMPC determined the cause of the event to be an inadequate
engineering
evaluation in 1984. A contributing factor was inadequate
design control.
Corrective actions included incorporation of the lessons learned from this event into
the engineering department continuing training program, and a review of other
radiation monitor set point calculations.
The inspectors discussed the modifications
with the CREVS system engineer and control room personnel,
and reviewed the
completed DERs, safety evaluation and the post-modification test, and had no
concerns.
This event was of low safety significance, in that, the emergency
4
18
procedures
require the operators to verify the CREVS is in operation, or to start the
system manually, in the event of a MSLB or LOCA. Notwithstanding, the failure
to properly evaluate the initiation logic for the CREVS is a violation of 10CFR50,
Appendix B, Criterion XI, "Test Control." This non-repetitive, licensee identified
and corrected violation is being treated as a Non-Cited Violation, consistent with
Section VII.B.1 of the NRC Enforcement Policy.
(NCV 50-220/98-05-05)
The inspectors verified that the LER was completed in accordance with the
requirements of 10CFR50.73.
This LER is closed.
Conclusions
During a review of the control room emergency ventilation system initiation logic,
NMPC determined that the system would not automatically initiate, as required.
Specifically, the system would not automatically start as a result of a main steam
line break or a loss of coolant accident.
This licensee identified and corrected
violation of 10CFR50, Appendix B, Criterion XI, "Test Control," was not cited.
Closed
LER 50-410 98-07: TS 3.0.3 Entr
Due to Missed Lo ic S stem
Functional Testin
of Loss of Volta e and De raded Volta e Channels
90712
The technical issues associated with this LER were described in Section E3.1 of IR
50-410/98-02.
The inspectors performed an in-office review and verified that the
LER was completed in accordance with 10CFR50.73.
This LER is closed.
Closed
Part 21 50-220 98-01: Defective GE SBM-T
e Switches at Unit 1
Ins ection Sco
e 36100
In January 1998, NMPC initiated a DER as a result of a GE Nuclear Energy (GENE)
.
Part 21 notification of an adverse condition related to the spring-return function of
some GE provided control switches that could damage the associated
control
circuits.
In March 1998, GENE issued
a revision to the notification explaining the
failure mode and root cause.
The inspectors reviewed the revised Part 21 and the
DER disposition.
Observations
Findin s and Conclusion
On March 19, 1998, GENE revised the Part 21 notification regarding
a failure of
some GE SBM-type control switches having a spring-return feature.
manufactures these switches as commercial grade.
The switches were purchased
as commercial grade and then dedicated for safety related applications by NMPC.
During the review of the original Part 21 notification, NMPC identified seven
potentially affected switches in safety-related functions for Unit 1 and NMPC
engineering initiated DER 1-98-0202.
The inspectors reviewed the revised Part 21 notification, the DER disposition, and
discussed the issue with the responsible maintenance
engineer.
GENE determined
19
the failure mechanism to be binding between the rear bearing and the casing
support caused
by shrinking of the casing support due to "post-mold cure."
The
mold for the casings had worn such that the bearing support hole was at the
minimum allowable value, and post-mold cure caused the hole to shrink. When
operated manually, the switch contacts operated properly.
GENE also determined
that switches in service for over two-years were not subject to the failure mode.
The licensee identified that all of the questionable switches at Unit 1 were greater
than two-years old, except one.
The inspector determined that the remote manual
control switch for the emergency cooling condenser vent to torus blocking valve
(the one exception) will be monitored until the two-year period is over.
The
inspector noted that it is NMPC's standard operating practice to verify that control
switches spring return to the normal position and that this verification may be
subject to peer (dual) verification.
The inspectors observed that NMPC's follow-up of the Part 21 report concerning GE
SBM-type control switches and their identification of the susceptible switches at
Unit 1 was thorough and an example of an improving questioning attitude by the
engineering staff. This Part 21 report is closed.
IV. PLANT SUPPORT
Using NRC IP 71750, the resident inspectors routinely monitored the performance
of activities related to the areas of radiological controls, chemistry, emergency
preparedness,
security, and fire protection.
Minor deficiencies were discussed with
the responsible management,
and significant observations
are detailed below.
R1
Radiological Protection and Chemistry (RP8cC) Controls
R1.1
Radiolo ical Environmental Monitorin
Pro ram Im lementation
a.
Ins ection Sco
e 84750
The following areas of the Radiological Environmental Monitoring Program (REMP)
were assessed
and reviewed:
selected sampling and analysis procedures,
analytical data from 1998,
selected sampling techniques,
operability and calibration of air samplers,
1996 and 1997 Land Use Census results,
1996 and 1997 Annual Radiological Environmental Operating Reports, and
licensee's investigation after identifying iodine-131 (I>>,) in milk in April 1997
C
1
20
Observations
and Findin s
The sampling and analysis procedures
provided appropriate guidance to perform
REMP tasks.
Sampling techniques were appropriate to collect environmental sample
media.
The air sampling equipment and water compositors were operable during
1997 to present,
as evidenced
in the sample logs and sample analysis results.
The
air sampling equipment calibration results were within the established tolerances,
and calibrations were performed within the frequency specified in the procedure.
A
Land Use Census was performed 1996 and 1997 during the growing season,
as
required by the TS.
The 1996 and 1997 Annual Radiological Environmental Operating Reports included
results of the environmental monitoring program, program changes,
land use
census,
and inter-laboratory comparison program, as required by TS. The reports
provided a comprehensive
summary of the results of the REMP around the site and
met the TS reporting requirements.
I)3$ was detected
in a routine indicator milk sample during the week of April 2 1
1997 at a concentration of 0.5 pCi/L. The licensee immediately conducted
an
investigation and discussed this issue with the NRC in April 1997. The primary
analytical contract laboratory immediately investigated the analysis results by re-
analyzing the sample and confirming the results with another laboratory.
The
investigation was detailed and exhaustive.
The licensee concluded that:
(1) the
source of the iodine could not be determined;
(2) that it was unlikely the source of
the I>>, was from either Nine Mile Point or from the J. A. FitzPatrick plant; and, (3)
the dose was insignificant compared to the doses received from natural sources.
The details and conclusions. of the investigation as a result of the I>>, was
documented
in the 1997 Annual Radiological Environmental Operating Report, as
.required by TS.
Conclusions
The licensee effectively maintained and implemented the Radiological Environmental
Monitoring Program in accordance with regulatory requirements.
The licensee
performed a comprehensive
review of an anomalous indication of I>>, in an
environmental milk sample.
Meteorolo ical Monitorin
Pro ram lm lementation
Ins ection Sco
e 84750
The inspectors reviewed the implementation of the meteorological monitoring
program (MMP); specifically, the status of the meteorological instrumentation
including, system operability, and the associated
channel calibration and channel
functional test procedures
and results were reviewed for the period of July 1996 to
May 1998.
I
0
21
Observations
and Findin s
Channel calibrations, channel checks, and channel functional tests were performed
within the frequency recommended
in Table 4.3.7.3-1 of TS 3/4.3.7.3 and
Regulatory Guide 1.23, Revision 1. The wind speed, wind direction, and
temperature
sensors
on the towers were operable; and applicable data was
available.
The associated
procedures
provided appropriate guidance to perform
channel functional tests and channel calibrations for all the channels, except for the
wind speed channels.
The required meteorological monitoring instrumentation channels (wind speed, wind
direction, and delta temperature)
shall be demonstrated
operable by the semi-annual
performance of the channel check and channel calibration operations,
as required by
TS 3/4.3.7.3.
Prior to May 22, 1998, NMPC had not performed a channel
calibration of the wind speed channel.
According to Unit 2 TS, Section 1.4, a
channel'calibration "... shall be the adjustment,
as necessary,
of the channel output
so that it responds with the necessary
range and accuracy to known values of the
parameter which the channel monitors.
The channel calibration shall encompass
the
entire channel including the sensor andalarm and/or trip functions, and shall include
the channel functional test."
Relative to wind speed, the licensee's calibration did
not include the wind speed sensor,
as required by the TS. Therefore, the accuracy
of the wind speed channel was not measured during channel calibrations.
Failure to
perform the channel calibration of the wind'speed channel, in accordance with the
Unit 2 TS, Section
1 4, constitutes
a violation of Unit 2 TS 3/4.3.7.3.
(VIO 50-410/98-05-06)
Conclusion
Overall, the licensee effectively maintained meteorological monitoring system
operability, and satisfactorily performed channel calibrations and channel functional
tests for the meteorological instrumentation, with the exception of the wind speed
channel.
The failure to'erform the channel calibration of the wind speed channel
according to the channel calibration definition of TS 1.4, in that, the accuracy of the
entire wind speed channel was not measured from the. sensor to the channel output,
constitutes
a violation of Unit 2 TS 3/4.3.7.3.
(VIO 50-410/98-05-06)
Unit 1 and Unit 2 Tours
Ins ection Sco
e 83750
A review was performed of housekeeping,
radiological boundaries,
and access
controls.
Information was gathered through tours of Unit 1 and Unit 2 reactor
buildings and drywells, and through discussions with cognizant personnel.
Observations
and Findin s
Housekeeping was adequate
in that walkways and aisles were clear and free of
debris, and major plant work areas were generally well illuminated. Some examples
22
of poor lighting were observed
in the Unit 2 drywell; reportedly due to a trip of a
temporary power breaker switch.
This was corrected the next day by re-
distributing several temporary lighting strings to another temporary power box.
High radiation areas and contaminated
areas were well delineated and clearly
posted.
A selective examination of the access to areas with dose rates greater than
1000 mrem per hour at 30 centimeters revealed appropriate controls, such as
locked doors or flashing lights. Access to radiologically controlled areas. was well
controlled with radiation work permits, health physics briefings, use of electronic
dosimetry, and radiological postings.
C.
Conclusion
Housekeeping
was adequate
in that aisles and walkways were clear and free of
debris, radiological boundaries and postings were clear, and access controls to
radiologically controlled areas were effective.
R1s4
Unit 2 Refuelin
Outa
e
a
~
Ins ection Sco
e 83750
A review was performed of radiological controls implemented for the Unit 2
refueling outage work. Specific areas evaluated included the refuel floor, drywell,
and suppression
pool. Information was gathered through tours of the facility,
interviews with cognizant personnel, attendance
at several drywell work scheduling
meetings, and selected examinations of reviews to maintain radiation exposures
as-
low-as-is-reasonably-achievable
(ALARA).
b.
Observations
and Findin s
Refuel'Floor:
ALARAReview No. 98-2-23, "Refuel Floor Activities," was used as
the major radiological control plan for work on the refuel floor. It included basic
ALARArequirements for refuel floor activities, and specific requirements for reactor
pressure vessel disassembly/reassembly,
underwater activities, and cavity/storage
pit decontamination.
The review was based on lessons learned during previous
outages and pertinent industry events.
The review included specific requirements
for work coordination, pre-job briefings, dose minimization, and contamination
controls.
The chief radiation protection (RP) technician maintained close oversight
of personnel access,
was thoroughly knowledgeable of ongoing work and
radiological controls, communicated well with plant work groups, and ensured that
personnel were instructed on radiological conditions and requirements prior to work.
~Dr well Major radiological controls for the drywall included close health physics
oversight of drywell access,
radiation work permits and ALARAreviews, extensive
use of temporary shielding, flushing of drain lines and reactor vessel nozzles, and
specific work planning and control. A chemical decontamination of the recirculation
system had been planned to minimize dose for recirculation valve work, but was
canceled when the system could not be fully isolated during the scheduled work
window. To compensate for this cancellation, several reactive drywell planning
23
meetings were conducted to establish
a revised work plan that accomplished
required work while minimizing radiation exposure.
Major station work groups
attended the meeting including outage planning, operations, maintenance,
engineering, and radiation protection.
Su
ression Pool:
Major work performed in the suppression
pool involved a
modification to replace emergency core cooling system suction strainers.
The
suction strainers were located below suppression
pool water level, requiring work to
be performed by divers.
Extremity dosimetry was issued to the divers in
accordance with procedural guidance,
and licensee actions including close oversight
by health physics personnel and use of administrative limits ensured that extremity
exposures were within regulatory and administrative limits. However, several
examples were identified in which the available administrative extremity exposure
limits were incorrectly determined and documented
on Procedure S-RPIP-5.4, "Dose
.Tracking and Timekeeping," Attachment 1: "Dose Tracking and Timekeeping
Worksheet."
Procedural guidance did not specify the exact method for determining
"available exposure," and several examples were identified in which the
administrative available exposure for the "extremity" was calculated by subtracting
the accrued whole body dose (rather than the accrued extremity dose) from the
administrative extremity dose limit.
The radiation protection manager acknowledged that the observed method for
determining the available administrative exposure for the extremity was incorrect,
and stated that instructions for determining the available administrative exposure for
the extremity would be clarified by a revision to procedure S-RPIP-5.4, "Dose
Tracking and,Timekeeping."
This failure constitutes
a violation of minor safety
significance and is not subject to formal enforcement action.
C.
Conclusions
Radiological controls for outage work were well planned and health physics
personnel maintained close oversight of work.
Procedure
S-RPIP-5 4, "Dose Tracking and Timekeeping," lacked clarity with regard
to the method for determining the available administrative extremity exposure,
and
several examples of inaccurate determinations of available administrative extremity
exposure were identified. The radiation protection manager stated that instructions
for determining the available administrative extremity exposure would be clarified by
a procedure revision,
R1.5
ALARAGoals and Initiatives
a 0
Ins ection Sco
e 83750
A review was performed of the use of goals to maintain radiation exposures
ALARA,and of ALARAinitiatives implemented for the Unit 2 refueling outage.
Information was gathered through reviews of ALARAgoals, tours of the plant,
J
P
24
discussions with cognizant personnel,
and a review of Safety Evaluation
No.98-040, "Chemical Decon of RCS."
b.
Observations
and Findin s
Outage exposure estimates were detailed, appeared
reasonable,
and were frequently
used to evaluate performance with regard to radiation exposure.
Exposure
estimates were established for work groups, major jobs, and the entire Unit 2
refueling outage.
To ensure the usefulness of the exposure goals, prompt changes
were made to reflect major changes
in work scope and cancellation of an attempted
chemical decontamination of the recirculation system.
The following examples of ALARAinitiatives were noted:
A camera monitor was set-up at the entrance to the radiologically controlled
area that allowed for viewing of multiple in-plant job locations including
specific drywell valves, under vessel areas,
and various locations of the
refueling floor.
A pre-outage ALARAr'eport was published that summarized radiological
control outage planning efforts. The document demonstrated
thorough
planning and preparation for outage work.
A chemical decontamination of the reactor recirculation system was planned
and set-up to reduce dose rates for major recirculation valve work. The
planned decontamination involved the low oxidation-state metal ion (LOMI)-
alkaline permanganate
(AP)-LOMI process (LOMI-AP-LOMI). However, the,
chemical decoritamination effort was canceled after water leakage through
the jet pump "ram" heads and through the pump discharge valve could not
be stopped during the scheduled work window.
Plans were in place to hydro wash eleven vessel nozzles including five
reactor
recirculation discharge nozzles, one jet pump instrumentation nozzle,
one HPCS nozzle, three feedwater nozzles, and one LPCI nozzle.
Numerous temporary shielding applications for job specific and general area
'ose
reduction were observed.
Examples included ten recirculation
discharge nozzles, the north scram dump column, and water shields for the
chemical decontamination resin columns.
c.
Conclusions
ALARAgoals were effectively used as a tool to aid radiological planning to minimize
radiation exposure,
Numerous ALARAinitiatives including publication of a pre-
outage report, use of cameras,
use of temporary shielding, planned reactor vessel
nozzle hydro washes,
and an attempt to chemically decontaminate the reactor
recirculation system demonstrated
management support and a commitment to
maintaining radiation exposures ALARA.
A
25
0
R7
Quality Assurance
in RP5C Activities
R7.1
Qualit
Assurance Audit Pro ram
a.
Ins ection Sco
e 84750
The inspector reviewed the following Quality Assurance
(QA) audit reports:
~
97015
~
96022
Environmental Protection, Radioactive Effluents, Radiological
Material Processing,
Transport and Disposal
Radiological Effluents, REMP, Offsite Dose Calculation Manual,
Radioactive Material Processing
b;
Observations
and Findin s
The objectives of the 97015 audit covered specific areas of the REMP and the
objectives of the 96022 audit covered specific areas of the REMP and MMP. Both
audits 'were conducted similarly. Previous DERs were reviewed and followed up for
completeness
and effectiveness of corrective actions.
The auditors reviewed
personnel performance, program implementation, and records.
No significant issues
were identified.
c.
Conclusion
The licensee met the QA audit requirements.
The audits were thorough and of
sufficient depth to assess
the REMP and MMP.
R7.2
Qualit
Assurance of Anal tical Measurements
a.
Ins ection Sco
e 84750
The following aspects of the Quality Assurance/Quality Control (QA/QC) program of
the primary contractor laboratory for the period of July 1996 to May 1998 were
reviewed:
~
the results of the internal QC program, including efficiency and resolution
checks, daily instrument energy checks, control charts of instrument
performance,
and routine calibrations; and
the results of the QA program, including the Inter-laboratory Comparison
(cross-check)
Program.
b.
Observations
and Findin
s
The QA/QC program for analyses of REMP samples
is conducted by the primary
analytical contract laboratory, J. A. FitzPatrick Environmental Laboratory.
The
laboratory implemented intra-laboratory (QC) and inter-laboratory (QA) programs.
The intra-laboratory (QC).program included efficiency and resolution, checks, daily
k
26
instrument energy checks, control charts of instrument performance,
and routine
calibrations.'he results for 1996 and 1997 were compiled and documented
in the
Environmental Laboratory QA/QC Report.
The results from 1996 through 1998
were within the acceptance
criteria. The laboratory continued to participate in an
Inter-laboratory Comparison Program provided by a vendor (Analytics, Inc.). The
laboratory's participation in this program was effective.
In addition to the above required comparison programs, the laboratory participated
in a cross check program with the Environmental Measurements
Laboratory (EML),
Department of Energy.
The analysis results of this program were generally in
agreement, with occasional disagreements
in certain samples.
The laboratory had
conducted
an investigation and determined the cause of the disagreements.
EML
provided sample media and geometries different from the usual sample media and
geometries provided by Analytics, Inc. and the licensee.
The laboratory
accommodated
and incorporated different and difficultmedia and geometries into
the program.
The licensee issued the 1997 Annual Radiological Environmental
Operating Report, as required by TS.
Conclusion
The contractor laboratory continued to implement effective QA/QC programs for the
REMP, and continued to provide effective validation of analytical results.
The
laboratory demonstrated
the ability to accommodate
and incorporate difficultmedia
and geometries into the program.
The programs were capable of ensuring
independent checks on the precision and accuracy of the measurements
of
radioactive material in environmental media.
Deviation Event Re orts and Self Assessments
Ins ection Sco
e 83750
A review was performed to evaluate methods used to identify, evaluate, and resolve
radiological control program deficiencies.
Information was gathered by a selected
review of radiological control issues documented
in DERs and a review of the self-
assessment
procedure.
Observations
and Findin s
The DER system had a high volume, low threshold, and the staff readily used the
system to address program deficiencies.
Ten DERs were selected to evaluate the
effectiveness of the system for resolving problems.
Problem evaluations including
identification of cause and corrective actions taken were reasonable
and
commensurate
with the significance of identified issues.
Self-assessment
Procedure NIP-ECA-05, "Posting and Surveys," was thorough in
that it included a review of radiation work permits, interviews with cognizant
personnel, extensive walkdowns of Unit 1 and Unit 2, and a compliance review with
respect to procedures
and the updated safety analysis report.
Assessment
team
L
27
members were well qualified and included four specialists, three supervisors, two
chief technicians,
and one peer evaluator from Diablo Canyon.
Numerous strengths
and opportunities for improvement were identified. Significant issues were placed
into the DER system, personnel were assigned to resolve identified issues,
and due
dates for completion were established.
A selected review of issues placed into the
DER system and interviews with responsible personnel indicated that adequate
progress was being made toward resolution of identified issues.
C.
Conclusions
C
The DER system and the self-assessment
program were effective in their use to
identify, evaluate, and resolve radiological program deficiencies.
S2
Status of Security Facilities and Equipment
S2.1
Tour of the Protected'Area
Perimeter
71750
The inspectors toured the Nine Mile Point Nuclear Station protected area perimeter
and found the fence and perimeter detection systems intact.
In addition, since the
tour was completed at approximately 1:30 a.m., the inspectors visually assessed
protected area lighting and found it to be acceptable.
S8
Miscellaneous Security and Safeguards
Issues
Process Software Altered 92904
S8.1
Closed
URI 50-220 5 50-410 96-06-06: Fitness-for-Dut
Random Selection
In May 1996, NMPC discovered that two contractors had intentionally altered the
fitness-for-duty (FFD) computer software code.
Specifically, the alteration excluded
the two individuals from the random selection process for FFD testing.
An
unresolved item was opened, pending completion of NMPC's internal investigation,
and subsequent
NRC review of the results.
S
On April 28, 1998, the NRC issued an enforcement action letter (EA 97-185) to
NMPC, stating that the failure to ensure that individuals were tested in a statistically
random and unpredictable manner was a violation of 10CFR26.24, and constituted
a Severity Level III violation. However, based on the NRC Enforcement Policy,
Section VII.B.6, the NRC decided to exercise discretion and not issue
a Notice of
Violation. (NCV 50-220 5 50-410/98-05-08)
Unresolved item 50-220 5 50-
410/96-06-06 is closed.
S8.2
Administrative Closure of Escalated Enforcement Items 92904
The below escalated
enforcement items (EEls) are being administratively closed,
based on the issuance of the enforcement action letter (EA 98-234), dated May 20,
1998, and the associated
determination:
28
EEI 50-220 & 50-410/98-01-01 was reclassified as a Level IV violation-
VIO 50-220 & 50-410/98-01-01
EEI 50-220 & 50-410/98-01-02was withdrawn
V. MANAGEMENTMEETINGS
X1
Exit Meeting Summary
At periodic intervals, and at the conclusion of the inspection period, meetings were
held with senior station management to discuss the scope and findings of this
inspection.
The exit meetings for specialist inspections were conducted upon
completion of their onsite inspection:
~
Environmental Monitoring
May 23, 1998
~
Outage Radiation Protection
May 23, 1998
The final exit meeting occurred on June 12, 1998.
During this meeting, the
resident inspector findings were presented.
NMPC did not dispute any of the
inspectors findings or conclusions.
Based on the NRC Region
I review of this
report, and discussions with NMPC representatives,
it was determined that this
report does not contain safeguards
or proprietary information.
~a
ATTACHMENT1
PARTIALLIST OF NMPC PERSONS CONTACTED
Nia ara Mohawk Power Cor oration
R. Abbott
D. Barcomb
D. Bosnic
J. Burton
H. Christensen
J. Conway
G. Correll
R. Dean
A. DeGracia
S. Doty
K. Dahlberg
G. Helker
A. Julka
P. Mezzafero
B. Murtha
L. Pisano
N. Rademacher
R. Randall
V. Schuman
R. Smith
C. Terry
C. Merritt
K. Ward
D. Wolniak
Vice President,
Nuclear Engineering
Manager, Unit 2 Radiation Protection
Manager, Unit 2 Operations
Manager, Training
Manager, Security
Vice President,
Nuclear Generation
Manager, Unit
1 Chemistry
Manager, Unit 2 Engineering
Manager, Unit 1 Work Control
Manager, Unit 1 Maintenance
Plant Manager, Unit 2 tActing)
Manager, Unit 2 Work Control
Director, ISEG
Manager, Unit 1 Technical Support
Manager, Unit 1 Operations tActing)
Manager, Unit 2 Maintenance
Manager, Quality Assurance
Manager, Unit I Engineering
Manager, Unit 1 Radiation Protection
Plant Manager, Unit
1
Vice President,
Nuclear Safety Assessment
&. Support
Manager, Unit 2 Chemistry
Manager, Unit 2 Technical Support
Manager, Licensing
New York Power Authorit
B. Gorman
D. Kiepper
A. McKeen
Environmental Supervisor, J. A. FitzPatrick Environmental Laboratory
I&C Manager
Radiological and Environmental Services Manager
Attachment
1 (cont.)
INSPECTION PROCEDURES USED
IP 37551
IP 61726
IP 71001
IP 71750
IP 84750
IP 92700
10 CFR Part 21 Inspections at Nuclear Power Plants
On-Site Engineering
Refueling Activities
Surveillance Observations
Maintenance Observations
Licensed Operator Re-qualification Program Evaluation
Plant Operations
Plant Support
Occupational Radiation Exposure
Radioactive Waste Treatment, and Effluent and Environmental Monitoring
In-Office Review of Written Reports of Non-Routine Events at Power
Reactor Facilities
Onsite Follow-up of Written Reports of Non-Routine Events at Power
Reactor Facilities
IP 92903
IP 93702
Follow-up - Maintenance
Follow-up - Engineering
Follow'-up - Plant Support
Prompt Onsite Response to Events at Operating Power Reactors
A-2
t
r<
Attachment
1 (cont.)
ITEMS OPENED
CLOSED AND UPDATED
OPENED
50-220/98-05-01
50-41 0/98-05-02
Failure to follow procedure, resulting in a missed plant
shutdown
Failure to conduct surveillance test on batteries
50-410/98-05-03
Failure to perform adequate
design for EDG modification
on fuel line
50-220/98-05-04
50-220/98-05-05
50-41 0/98-05-06
Failure to maintain secondary containment integrity
Failure to properly evaluate control room emergency
ventilation s stem initiation lo ic
y
g
Failure to perform calibration of wind speed channel
50-220 5
50-410/98-05-08
Failure to ensure individuals were randomly tested for
fitness-for-duty
CLOSED
50-220/98-05-04
50-220/98-05-05
50-220 5
50-41 0/98-05-08
50-220/96-01-03
50-220 8L
50-41 0/96-01-05
50-220 5.
50-41 0/96-06-06
NCV
Failure to maintain secondary containment integrity
Failure to properly evaluate control room emergency
ventilation system initiation logic
Failure to ensure individuals were randomly tested for
fitness-for-duty
Lack of Testing of control room annunciators
Failure to perform safety evaluation prior to installation of
Apparent Tampering of fitness-for-duty computer
50-410/96-1 0-03
VI0
Procedure changes not in accordance with TS
requirements
50-220 5
50-41 0/96-1 4-02
50-41 0/97-02-02
50-220/97-1 2-08
50-220/98-05
50-220/98-06
50-41 0/98-05
LER
LER
LER
Over-pressurization
concerns relative to GL 96-06
Missed TS surveillance on HPCS actuation
instrumentation
Impact of drywell-to-wetwell bypass on containment
pressure
Unrecognized Violation of TS Secondary Containment
Design Deficiency Associated with Control Room
Emergency Ventilation System Radiation Monitors
Reactor Water Cleanup Isolation on High Differential Flow
Caused by Relief Valve Lifting
A-3
la
Attachment
1 (cont.)
CLOSED
50-41 0/98-06
50-41 0/98-07
50-41 0/98-08
50-41 0/98-09
50-41 0/96-1 0-01
50-220/98-01
UPDATED
LER
LER
LER
LER
Part 21
Engineered Safety Feature Actuations Due to Partial Loss
of Offsite Power
TS 3.0.3 Entry Due to Missed Logic System Functional
Testing of Loss of Voltage and Degraded Voltage
Channels
HPCS Out of Service with One Division RHS in
Suppression
Pool Cooling
Missed Battery Technical Specification Surveillance
Requirements
Due to Inappropriate Interpretation
Post-maintenance
testing of Unit 2 MSLRM
Defective GE SBM-Type Switches at Unit 1
50-220 5.
50-41 0/98-08-01
Failure to properly control, store, and classify safeguards
information - changed to VIO 50-220 5 50-410/98-02-01
WITHDRAWN
50-220 8L
50-41 0/98-08-02
Failure to report an event in accordance with
A-4
Attachment
1 (cont.)
LIST OF ACRONYMS USED
cpm
CFR
DER
EML
GENE
GL
~is~
IR
LCO
LER
MMP
NRC
Part 21
RBEVS
RP5C
SORC
As Low As Is Reasonably Achievable
counts per minute
Code of Federal Regulations
Control Room Emergency Ventilation System
Deviation/Event Report
Enforcement Action
Escalated Enforcement Item
Environmental Monitoring Laboratories
Engineered Safeguards
Feature
General Electric Nuclear Energy
Generic Letter
High Pressure
Iodine 131
Inspection Report
Limiting Condition for Operation
Licensee Event Report
Loss of Coolant Accident
Low Pressure
Coolant Injection
Meteorological Monitoring Program
Main Steam Line Break
Non-Cited Violation
Niagara Mohawk Power Corporation
Notice of Enforcement Discretion
Nuclear Regulatory Commission
Quality Assurance
Quality Control
Procedure Change Evaluation
Reactor Building Emergency Ventilation System
Radiological Effluents Monitoring Program
Refueling Outage
Residual Heat Removal System
Radiological Protection 5. Chemistry
Spent Fuel Pool
Station Operating Review Committee
Senior Reactor Operator
Station Shift Supervisor
Tube Exchanger Manufacturer's Association
A-5
Attachment
1 (cont.)
TS
TSSR
Unit 1
Unit 2
Technical Specification
Technical Specification Surveillance Requirement
Updated Final Safety Analysis Report
Nine Mile Point Unit 1
Nine Mile Point Unit 2
Unresolved Item
Violation
Work Order
A-6
f'