ML17059B782
| ML17059B782 | |
| Person / Time | |
|---|---|
| Site: | Nine Mile Point |
| Issue date: | 11/24/1997 |
| From: | Doerflein L NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I) |
| To: | |
| Shared Package | |
| ML17059B780 | List: |
| References | |
| 50-220-97-07, 50-220-97-7, 50-410-97-07, 50-410-97-7, NUDOCS 9712090013 | |
| Download: ML17059B782 (80) | |
See also: IR 05000220/1997007
Text
U.S. NUCLEAR REGULATORYCOMMISSION
REGION I
Docket/Report Nos.:
50-220/97-06
50-410/97-06 i
License Nos.:
NPF-69
Licensee:
Niagara Mohawk Power Corporation
P. O. Box 63
Lycomnin, NY 13093
Facility:
Nine Mile Point, Units
1 and 2
Location:
Scriba, New York
Dates:
August 10 - October 4, 1997
Inspectors:
B. S. Norris, Senior Resident Inspector
T. A. Beltz, Resident Inspector
L. L. Eckert, Radiation Specialist
J. T. Furia, Senior Radiation Specialist
M. L. Hart, NRR Intern
J. R. M'Fadden, Radiation Specialist
T. A. Moslak, Project Engineer
L. A. Peluso, Radiation Physicist
R. A. Skokowski, Resident Inspector
Approved by:
cx
Lawrence T. Doerflein, Chief
Projects Branch
1
Division of Reactor Projects
l i /P 'I /1 "1
Date
97i20900i3 97ii28
ADOCK 05000220
8
TABLE OF CONTENTS
TABLE OF CONTENTS
page
EXECUTIVE SUIVIMARY
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VI
SUMMARYOF ACTIVITIES...
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Niagara Mohawk Power Corporation (NMPC) Activities
1
Nuclear Regulatory Commission (NRC) Staff Activities ..............
1
I. OPERATIONS
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Conduct of Operations
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01.1
General Comments
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01.2
NMP1 Reactor Shutdown due-to Emergency Cooling (EC)
Condenser Tube Leak................
02
Operational Status of Facilities and Equipment
02.1
NMP2 Standby Liquid Control System Engineered Safety Feature
Walkdown.... ~................
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02.2
Plant Walkdowns..................................
08
Miscellaneous Operations Issues .....
08.1
(Closed) IFI 50-220/96-07-18 5 50-410/96-07-18:
Material
Condition Discrepancies Identified in Several Areas ..........
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II. MAINTENANCE
M1
Conduct of Maintenance...
M1.1
General Comments......
M1.2
Repairs to NMP1 Emergency Cooling Condensers
M1.3
NMP2 Maintenance Activities on Offsite Power Supply
M7
Quality Assurance
in Maintenance Activities ..
M7.1
Missed Surveillance Test of the NMP1 Control Room Ventilation
Radiation Monitor ..
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Miscellaneous Maintenance Issues
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M8.1
(Closed) URI 50-220/96-07-04:
Procedure
Change Evaluation
Used to Change Intent of a NMP1 Procedure
M8.2
(Closed) LER 50-410/97-06:
Plant Shutdown Due to Rising
M8.3
(Closed) LER 50-410/97-07:
Failure to Calibrate Hydrogen
Recombiner Instruments as Required by Technical Specifications
Due to Procedure Omission
III. ENGINEERING......... ~...... ~..........
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Conduct of Engineering ~...... ~.................
E1.1
General Comments... ~...
EB
Miscellaneous Engineering Issues
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E8.1
(Closed) EA 96-079/VIO 1013:
Design Control Measures
Inadequate
during Calculations for Establishing Reactor Building and
Turbine Building Relief Pressure
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Table of Contents (cont'd)
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E8.2
(Closed) URI 50-220/96-05-01:
NRC Staff Review of Revised
Reactor Building and Turbine Building Blowout Panel Relief
Pressure
Calculations ..
E8.3
(Closed) IFI 50-220/96-05-02:
Inconsistencies
in the NMP1
UFSAR and IPE with respect to the Reactor Building and Turbine
Building Blowout Panel Relief Pressure Setpoints.............
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E8.4
(Closed) LER 50-220/97-07:
Potential Control Room Emergency
Ventilation System Operation Outside the Design Basis due to
Inadequate
Evaluation
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IV. PLANT
R1
R2
R3
R5
R7
S1
F2
SUPPORT
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Radiological Protection and Chemistry (RP&C) Controls .............
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R1.1
General Comments.... ~...
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R1.2
Radiological Protection Program ..
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R1.3
Transportation and Radiological Waste Programs.............
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R'l.4
Shipment of Radioactive Material to an Unlicensed Facility . ~.... 21
Status of RP&C Facilities and Equipment ................
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R2.1
Radiological Protection Facilities and Contamination Controls
Instrumentation ~... ~, ~....,
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PR&C Procedures
and Documentation .........................
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R3.1
Shipment of Wrong Radwaste Material
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Staff Training and Qualifications .... ~................. ~.... 25
R5.1
Training of Staff Involved in Radioactive Material Transportation
and Radwaste Processing........ ~........ ~..........
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Quality Assurance
(QA) in RP&C Activities...................
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R7.1
QA in Radiation Protection Activities
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R7.2
QA in Radiological Transportation and Radwaste Activities ..'.... 26
Conduct of Security and Safeguards Activities
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S1.1
General Comments
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S1.2
Unusual Event - Discovery of a Suspicious Package...... ~.... 28
Status of Fire Protection Facilities and Equipment
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F2.1
Control Room Fire Suppression
System and Operator Response
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V. MANAGEMENTMEETINGS....
X1
Exit Meeting Summary .....
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ATTACHMENT1
- PARTIALLIST OF PERSONS CONTACTED
- INSPECTION PROCEDURES USED
- ITEMS OPENED, CLOSED, AND UPDATED
- LIST OF ACRONYMS USED
EXECUTIVE SUMMARY
Nine IVlile Point Units 1 and 2
50-220/97-06 & 50-410/97-06
August 10 - October 4, 1997
This integrated NRC inspection report includes reviews of licensee activities in the
functional areas of operations, engineering, maintenance,
and plant support.
The report
covers an eight-week period of inspections and reviews by the resident inspectors,
and
regional specialists in the areas of radioactive waste processing, radioactive material
transportation and radiation protection.
PLANT OPERATIONS
The questioning attitude of a Nine Mile Point Unit 1 (NMP1) chemistry technician and the
heightened sensitivity of the NMP1 staff to the possibility of an emergency cooling (EC)
condenser tube leak were good.
During the ensuing reactor shutdown, the control room
operators'se
of alarm response
procedures, three-part communications, and self/peer
checking were noticeably improved.
Special simulator training resulted in good operating
crew performance during the manual reactor shutdown.
The system walkdowns and performance history reviews indicated that the material
condition of the Nine Mile Point Unit 2 (NMP2) standby liquid control system was good,
and that the system has demonstrated
a high level of reliability. The knowledge level of
the technicians and operators during the performance of an observed surveillance test was
good.
However, operators stepping on small diameter piping and using a pipe wrench to
assist in the manual valve manipulation indicated poor work practices, in that their actions
could potentially damage plant equipment.
NMP2 operators considered
a catch containment used to collect oil leaking from a gear box
on the reactor core isolation cooling pump to be a permanent installation.
However,
contrary to NMPC procedure,
a plant change request had not been initiated.
(NCV)
IVIAINTENANCE
During NMP1 emergency cooling condenser repair activities, foreign material exclusion
controls were appropriately maintained, in that material accountability and system
cleanliness were controlled.
Maintenance personnel adhered to work order requirements,
and all associated
procedures
and documentation were readily available and the current
revision.
During a pipe cutting evolution, a poor safety and radiological work practice was
identified, in that maintenance
personnel were using a rubber-gloved hand to remove metal
shavings.
Radiological controls were satisfactory.
Quality assurance
(QA) oversight of
ongoing maintenance activities was appropriate.
Inattention-to-detail and failure to self-check a completed surveillance test data sheet by
NMP1 radiation protection (RP) calibration staff resulted in the failure to perform a
ventilation radiation monitor instrument channel calibration within the technical
specification (TS) required frequency.
(VIO)
Executive Summary (cont'd)
The inspectors considered the discovery by the NMP2 instrumentation and control
technicians of the missing calibrations in the hydrogen recombiner system to be good.
However, this was another example of a missed TS surveillance.
(VIO)
ENGINEERING
An NRC review, in 1996, of the calculations to support the modification to bring the NMP1
blowout panels within the design basis identified minor calculational errors.
In addition,
NRC noted that corrective actions in early 1996 related to the NMP1 blowout panels
design control concern had not been fullyeffective.
(NCV)
An NMP1 operator's questioning attitude of the control room smoke purge system was
very good and resulted in an engineering operability evaluation of the impact on control
room emergency ventilation system (CREVS) operability. Notwithstanding, the interface
between the smoke purge system and CREVS was inadequately evaluated during
modifications in the early 1980s.
(NCV)
PLANT SUPPORT
The radiation protection (RP) program area was being well-implemented at both units.
The
NMP1 outage ALARA(as-low-as-reasonably-is-achievable)
goal was exceeded
due to
emergent work. Very good radiological housekeeping
was noted in NMP2. Effective
programs were implemented for contamination control and external dosimetry.
The quality
assurance
(QA) program for the above areas was well implemented; audits and self-
assessments
were of appropriate scope and technical depth.
At both units, a good program had been established for the processing of liquid and solid
radioactive waste (radwaste); although the Process Control Programs (PCPs) and
associated
procedures
have not been properly maintained.
(EEI) Also, the lay-up of the
NMP1 ¹11 waste concentrates
tank was questionable;
NMPC indicated they would review
this issue and provide the NRC with an action plan to deal with it.
(IFI) At NMP2, plant
conditions were generally very good relative to radiological housekeeping
in radwaste.
However, the QA program failed to identify fullythe defects within the unit specific PCPs,
and in one instance failed to ensure that corrective actions were taken to address
an
identified defect.
(EEI) Additionally, a number of required audits of vendors providing
transportation and/or waste services were not performed.
(EEI) The above apparent
violations are being considered for escalated enforcement, and are indicative of a lack of
attention by management
in this area.
On three different occasions during this inspection period, NMPC inadequately controlled
shipments of radiological material to facilities offsite.
(1) The shipment of a sample from
the NMP1 core shroud shifted during transport and caused the radiation levels in the
occupied space of the truck to exceed limits. (EEI) (2) A wrong liner of low-level radwaste
was shipped offsite for disposal.
(EEI)
(3) A sample from the NMP1 EC condenser was
shipped to an unlicensed facility; in addition, a similar occurrence happened
in 1995. (EEI)
Allof the examples appeared to be due to a lack of procedures describing radwaste
Executive Summary (cont'd)
operator activities, inattention-to-detail, and a lack of supervisory oversight.
The above
apparent violations are being considered for escalated
enforcement.
The response of the Nine Mile Point security personnel to a "suspicious looking" package
was acceptable.
The declaration of an Unusual Event by the NMP2 SSS was appropriate
and in accordance with the NMP2 Emergency Plan.
The inspectors noted that the concern associated with the automatic fire suppression
system actuation in the control room of another nuclear power plant did not exist at Nine
Mile Point.
Plant personnel appeared trained and equipped to combat a control room fire.
Additionally, procedures were in place should personnel evacuation of the control room be
required.
REPORT DETAILS
Nine Mile Point Units 1 and 2
50-220/97-06 8( 50-410/97-06
August 10 - October 4, 1997
SUIVIIVIARYOF ACTIVITIES
Niagara IVlohawk Power Corporation (NIVIPC) Activities
Nine Mile Point Unit 1 (NMP1) started the inspection period at full power.
On
September
15, 1997, the unit was shutdown due to indications of a tube leak in
emergency cooling (EC) condenser ¹122.
Subsequently,
tube leaks were identified in all
four EC condensers.
NMP1 was shutdown for the remainder of the inspection period while
NMPC investigated the root cause of the tube leaks and evaluated repair options.
NMP2
Nine Mile Point Unit 2 (NMP2) started the inspection period in the startup mode, following
a forced outage to repair a leaking flexible drain hose on the "8" recirculation flow control
valve.
NMP2 obtained 95% of rated full power on August 12, 1997; power was limited to
95% due to the moisture separator reheaters
being isolated. On September 7, power was
reduced to 55% for a feedwater pump exchange.
Power restoration was delayed due to
equipment problems with a feed water heater level control valve; repairs were completed
and 95% power was achieved on September 10, 1997.
NMP2 maintained essentially 95%
power for the remainder of the inspection period.
Nuclear Regulatory Commission (NRC) Staff Activities
Ins ection Activities
The NRC conducted inspection activities during normal, backshift, and deep backshift
hours.
In addition to the inspection activities completed by the resident inspectors,
regional specialists conducted inspections and reviews in the areas of radioactive waste
(radwaste) processing, radioactive material transportation,
and radiation protection.
The
results of the specialist inspections are contained in the applicable sections of this report.
In addition, an inspection of the security program was completed near the end of this
period, the results of that inspection will be included in the IR 50-220 5 50-410/97-11.
Three other NRC inspections were completed during this period, and are documented
in
separate
inspection reports (IRs):
Corrective Actions Program:
IR 50-220/97-805 50-410/97-80
Engineering and Closure of Generic Letter 89-10 Issues:
IR 50-220/97-095
50-410/97-09
Program and Full Participation Exercise:
IR 50-220/97-10
5 50-410/97-10
U dated Final Safet
Anal sis Re ort Reviews
A discovery of a licensee operating their facility in a manner contrary to the Updated Final
Safety Analysis Report (UFSAR) description highlighted the need for additional verification
that licensees were complying with UFSAR commitments.
While performing the
inspections discussed
in this report, the inspectors reviewed the applicable portions of the
UFSAR related to the areas inspected.
The inspectors verified that the UFSAR wording
was consistent with the observed plant practices, procedures and/or parameters, with
exception of the radwaste program as described in Section R1.3 of this report.
I. OPERATIONS
01
Conduct of Operations (71707)
'1.1
General Comments
Using NRC Inspection Procedure 71707, the resident inspectors conducted frequent
reviews of ongoing plant operations.
Specialist inspectors in this area used other
procedures
during their reviews of operations activities; these inspection procedures
are listed, as applicable, for the respective sections of the inspection report.
In
general, the conduct of operations was professional and safety-conscious;
specific
events and noteworthy observations
are detailed in the sections below.
01.2
NMP1 Reactor Shutdown due to Emer enc
Coolin
EC Condenser Tube Leak
a e
Ins ection Sco
e
The inspectors assessed
the licensee's actions in response to indications of a tube
leak in EC condenser ¹122. The assessment
included a review of the EC system
atmospheric vent radiation monitor data, chemistry sample results, operator logs,
applicable portions of the UFSAR, and discussions with various members of the
licensee's staff.
The inspectors observed control room activities during the reactor
shutdown, including a review of the applicable procedures
and technical
specifications (TS). Also, the inspectors monitored the initial actions of the licensee
to identify the location of the leak.
S stem Descri tion
The NMP1 EC system is a passive, standby system designed to remove decay heat
from the reactor, following a reactor scram, without the loss of reactor water
inventory.
The EC system is used as a heat sink when the main condenser
is not
available.
Upon initiation, steam from the reactor passes
through the EC condenser
tubes and returns to the reactor as water.
The EC system consists of two
independent
loops, with two condensers
per loop.
1 Topical headings such as 01, M8, etc., are used in accordance with the NRC standardized reactor inspection report outline.
Individual reports are not expected to address
all outline topics.
The NRC inspection manual procedure or temporary instruction
ITI) that was used as inspection guidance is listed for each applicable report section.
Observations
and Findin s
On the evening of September
11, a NMP1 chemistry technician observed that the
steam vapor from the EC loop ¹12 atmospheric vent was slightly more than normal.
At 10:45 p.m., the chemistry technician further determined that radiation levels
were higher than normal in the area of the EC condensers.
The technician informed
the NMP1 Station Shift Supervisor (SSS) of the observation, and was directed to
sample the EC loop ¹12,
On September 12, at about 1:30 a.m., NMP1 control
room operators noted that the shell-side temperature for ¹122 had increased,
and
the vent radiation monitor reading for EC loop ¹12 had also increased slightly, both
indicative of a tube leak in an EC condenser.
Subsequently,
chemistry results
verified a tube leak.
Based on the indications, operators isolated EC loop ¹12, and
noted that the associated
vent radiation monitor reading returned to normal.
Deviation/Event Report (DER) 1-97-2669 was initiated to investigate the concern.
The inspectors considered the questioning attitude of the chemistry technician, and
the heightened sensitivity of the NMP1 staff to the possibility of EC condenser tube
leaks to be good.
Additionally, the inspectors found the actions taken for the
potential EC condenser tube leak to be appropriate, and consistent with the actions
described in the UFSAR.
On September
14, with EC loop ¹12 isolated from the reactor coolant system,
NMPC attempted to hydrostatically test the tubes in EC condenser ¹122, in
accordance with an approved procedure.
In preparation for the hydrostatic test,
operators began to fillthe tubes with water prior to pressurizing the system and
noted that the water level was rising in the shell side of the condenser.
This
confirmed that a tube leak existed in EC condenser ¹122.
Based on these
indications, NMPC decided further investigation was required and NMP1 was
shutdown on September 15.
The inspectors observed the NMP1 control room activities during the reactor
shutdown.
Control room operators performed the shutdown in accordance with
approved procedures,
and it was completed without incident. The inspectors noted
that the use of alarm response
procedures
and three-part communications,
in
addition to self/peer checking, was improved.
This was the first shutdown of NMP1, within approximately five years, using
manual insertion of all control rods.
Previously, planned shutdowns were completed
by inserting control rods to a power level of approximately 20%, at which time a
manual scram was initiated to complete the reactor shutdown.
NMPC performed
the shutdown without a manual scram to minimize impact on the control rod drive
(CRD) seals, and to determine whether CRD performance following this shutdown
would be better than after past manual scrams.
Due to the extended length of time
since the last manual reactor shutdown, the operating crew scheduled to complete
the evolution practiced the procedure on the simulator.
The inspectors considered
the simulator training to be of value, as evidenced by the good performance of the
operating crew during the actual reactor shutdown.
On September
16, using a boroscope,
NMPC identified a 1-inch break on an inlet
tube in EC condenser ¹122.
To obtain insights as to when the tube leak might have
initiated, the inspectors reviewed historical data for the EC system, particularly
chemistry sample and vent radiation monitor readings.
The inspectors reviewed the
gamma spectrum analysis data from water samples taken from the shell side of the
condenser,
and discussed the results with the NMP1 Chemistry Manager.
The data
included routine monthly samples for August and September,
and the sample drawn
on September
11 subsequent
to the event.
EC condenser vent radiation monitoring
strip recorder data was also reviewed by the inspectors.
The data included both
trains of EC condensers
from September 9 through September
11. The Loop ¹12
vent radiation monitor data indicated a noticeable increase
in radiation levels
beginning on the afternoon of September
11, an approximate 0.3 milliroentgen per
hour (mR/hr) increase.
The maximum indicated radiation level was 1.1 mR/hr on EC
condenser ¹122, the alarm setpoint is 5 mR/hr; the indicated radiation levels were
well below the allowed release limits Title 10 of the Code of Federal Regulations,
Part 50 (10 CFR 50), Appendix I. The inspectors noted that all of the data,
including the gamma spectrum analysis, indicated that the condenser tube failure
occurred sometime between September
9 and 11.
During a subsequent
hydrostatic test, NMPC also identified tube leaks in EC
condensers ¹111, ¹112, and ¹121. As of the close of this inspection period,
NMPC was in the process of determining the extent of the tube leaks, and
investigating the failure mode and the root cause of the tube leaks.
management
indicated the repair and corrective actions would be based on results
of the investigation.
C.
Conclusions
The questioning attitude of the NMP1 chemistry technician and the heightened
sensitivity of the NMP1 staff to the possibility of an EC condenser tube leak were
good.
During the ensuing reactor shutdown, the operators'se
of alarm response
procedures, three-part communications, and self/peer checking were improved.
Special simulator training resulted in good operating crew performance during the
reactor shutdown.
02
Operational Status of Facilities and Equipment (71707)
02.1
NMP2 Standb
Li uid Control S stem En ineered Safet
Feature Walkdown
Ins ection Sco
e
The inspectors assessed
the ability of the standby liquid control (SLS) system to
perform its intended function. This assessment
included a visual inspection
(walkdown) of accessible
portions of the SLS system.
The inspectors observed
performance of one surveillance test and reviewed several completed surveillance
tests associated with the SLS system.
The inspectors reviewed the SLS "System
Health" report, and applicable sections of the NMP2 UFSAR, the TSs, the Individual
Plant Examination (IPE), and the operating procedures.
The inspectors also
reviewed the SLS system with respect to the Maintenance Rule, Title 10 of the
Code of Federal Regulations, Part 50.65 (10 CFR 50.65).
During the assessment,
the inspectors discussed the related issues with the system engineer, chemistry
department supervisor, operators,
Operations Management,
and the NMP2
Maintenance
Rule Coordinator.
S stem Descri tion
The NMP2 SLS system provides a method to chemically shutdown the reactor.
It is
used only in the event that a sufficient number of control rods cannot be inserted
into the reactor core to shutdown the reactor.
The SLS system shuts down the
reactor by injecting a neutron absorbing boron solution into the reactor coolant
system.
The
SLS system consists of a storage tank that provides the boron
solution to two divisions of components.
Each division includes a positive
displacement pump, an explosive valve, a motor-operated valve (MOV), and
associated
manual valves, piping and controls.
Both divisions use a common header
that connects to the high pressure core spray (HPCS) system, downstream of the
inboard containment isolation valve. The boron solution is discharged radially over
the top of the core through the HPCS sparger.
The SLS system can be manually
initiated from the control room, or automatically initiated by the redundant reactivity
control system.
Observations
and Findin s
The inspectors performed a walkdown of accessible
portions of the SLS system.
The inspectors compared plant drawings and Procedure N2-OP-36A, "Standby
Liquid Control System," Revision 4, to the actual valve positions; no discrepancies
were identified.
In general, the material condition of the equipment appeared to be
good.
The inspectors identified no current valve leakage; however, the inspectors
noted four manually-operated
valves with minor visible indication of boron
encrustation.
Subsequently,
the inspectors ascertained that the licensee had
already planned to clean and inspect two of these valves the following week.
The
inspectors provided the licensee with the other two valve numbers and the licensee
added them to their scheduled work. Housekeeping
and equipment labeling were
generally good.
The inspectors identified two valves without the standard
component identification label; upon informing the system engineer, actions were
taken to obtain the proper labels.
The inspectors compared the design of the SLS system to the description provided
in the UFSAR and identified no discrepancies.
The UFSAR states that the usable
volume of the SLS system boron solution storage tank is 5.1 inches above the
centerline of the tank outlet piping, rather than from the bottom of the tank.
The
inspectors verified that appropriate tank levels and volumes were considered
in
applicable chemistry procedures
and instrumentation calibration instructions.
The inspectors reviewed completed surveillance tests associated with the SLS
system.
The inspectors determined that the tests adequately included surveillance
and testing requirements described
in the TSs and UFSAR. The inspectors observed
SLS system surveillance test N2-OSP-SLS-0001, "Standby Liquid Control Pump,
Check Valve, Relief Valve Operability Test and 40 Month Functional Test,"
Revision 6, for Division II, performed September 2, 1997.
The surveillance test was
satisfactorily completed.
Based on the response to inspectors'uestions,
the
knowledge level of the operators and technicians performing the test appeared to be
good.
However, the inspectors noted two deficiencies during the performance of
the surveillance test:
~
The first was that the operators occasionally stepped on small diameter
piping, although no damage was done in this instance.
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The second was that the operators used a pipe wrench to manipulate the
SLS pump flow test throttle valve (2SLS" HCV116). The condition of the
handwheel indicated that this had occurred in the past.
The inspectors discussed these concerns with the NMP2 Operations Manager.
He
agreed there was a potential for equipment damage,
and provided direction (via the
"Night Notes" ) to the operating crews, emphasizing the importance of (1) not
walking on small diameter piping, and!2) contacting the SSS if difficultyis
experienced during valve manipulations.
In addition, the system engineer issued a
problem identification (PID) report to investigate the difficultoperation of the valve.
The inspectors reviewed the current "System Health Report" for SLS, and discussed
system performance with the system engineer.
There was no indication of major
corrective maintenance for the system.
Additionally, the inspectors verified that the
SLS system was performing within the maintenance
rule-established
acceptance
criteria.
Conclusions
The system walkdowns and performance history reviews indicated that the material
condition of the SLS system was good, and that the system has demonstrated
a
high level of reliability. The knowledge level of the technicians and operators during
the performance of an observed surveillance test was good.
However, operators
stepping on small diameter piping and using a pipe wrench to assist in the manual
valve manipulation indicated poor work practices, in that their actions could
potentially damage plant equipment.
Plant Walkdowns
The inspectors conducted routine tours of both units during this inspection period.
Following the shutdown of NMP1, the inspectors toured the feedwater heater and
condenser bays and other areas normally inaccessible
during power operation.
Overall, the inspectors noted that equipment material condition and compartment
housekeeping
at both units were acceptable;
although, during the tours, some minor
discrepancies
were noted.
These discrepancies
were discussed with licensee
management
and corrected.
During a tour of the NMP2 reactor core isolation cooling (RCIC) room, the inspectors
noted a tygon tube directing oil leakage from a gear box to a metal catch
containment.
Although this was being tracked through the licensee's catch
containment program (catch containment 97-02-14), no PID or work order (WO) had
been generated to repair the leak.
Discussions with the onshift SSS indicated that
the operators emptied the containment as necessary
and accepted this as
permanent.
The inspectors discussed
the issue with the NMPC fire protection
supervisor and verified that the oil contained within the containment would not
cause the fire loading within the RCIC room to be exceeded.
The inspectors'iscussion
with the NMP2 General Supervisor of Operations (GSO)
and review of Procedure GAP-OPS-04, "Catch Containments," Revision 2, indicated
that permanently installed catch containments needed to be evaluated
as
modifications. Through the GSO, the inspectors ascertained that catch containment
97-02-14 was not evaluated as a modification. As a result of the inspectors
questions,
a plant change request was initiated by the system engineer.
The failure
to evaluate the catch containment as a modification is a violation of the TS 6.8.1,
regarding procedure adherence.
This failure constitutes
a violation of minor
significance and is being treated as a Non-Cited Violation (NCV), consistent with
Section IV of the NRC Enforcement Policy. (NCV 50-410/97-07-0'l)
08
Miscellaneous Operations Issues (90712,92700)
08,1
Closed
IFI 50-220 96-07-18 & 50-410 96-07-18: Material Condition
Discre ancies Identified in Several Areas
During the NRC Integrated Performance Assessment
Process
(IPAP) team
inspection, several material condition discrepancies
associated with the NMP1
shutdown cooling pumps, the NMP2 chilled water pumps, and the NMP2 emergency
diesel generators were noted.
The inspectors routinely tour all accessible
areas of
both units.
During this inspection period, the inspectors specifically examined the
above equipment, and identified no major discrepancies.
Minor problems and
general housekeeping
concerns were discussed with the onshift SSS and corrected.
This item is closed.
II. MAINTENANCEa
Conduct of Maintenance (61726, 62707)
General Comments
Using NRC Inspection Procedures 61726 and 62707, the resident inspectors
periodically observed plant maintenance activities and the performance of various
surveillance tests.
As part of the observations, the inspectors evaluate the activities
Surveillance activities are included under "Maintenance."
For examplo, a section involving surveillance observations
might
be included as a separate sub-topic under Mt, "Conduct of Maintenance."
with respect to the requirements of the Maintenance
Rule, as detailed in Title 10 of
the Code of Federal Regulations, Part 50.65 (10CFR50.65).
Specialist inspectors in
.
this area used other procedures
during their reviews of maintenance
and
surveillance activities; these inspection procedures
are listed, as applicable, for the
respective sections of the inspection report.
In general, maintenance
and
surveillance activities were conducted professionally, with the work orders (WOs)
and necessary
procedures
in use at the work site, and with the appropriate focus on
safety.
Specific activities and noteworthy observations
are detailed in the
inspection report.
The inspectors reviewed procedures
and observed all or portions
of the following maintenance/surveillance
activities:
~
N2-ISP-HCS-R1 10
~
N2-CSP-SLS-M110
~
N2-CSP-SLS4112
~
N2-OSP-SLS-CS001
~
N2-OSP-SLS-Q001
~
N2-OSP-SLS-0002
~
N2-OSP-SLS-R001
~
N2-OSP-SLS-R002
~
N2-OSP-LOG-D001
~
WO 96-01 105-02
WO 96-01 530-02
~
WO 97-04407-00
~
WO 97-04407-23
~
WO 97-04629-08
~
WO 95-01432-08
Operating Cycle Channel Calibration of the Recombiner
Reactor Temperature Instrumentation
Standby Liquid Control Monthly Surveillance
Adjustment of SLS [Standby Liquid Control] Tank
Sodium Pentaborate
Concentration
SLS Injection Header Check Valve Reverse Flow Test
Standby Liquid Control Pump, Check Valve, Relief
Valve Operability Test and 40 Month Functional Test
Standby Liquid Control Valve Operability Test
Standby Liquid Control Manual Initiation Actuation and
40 Month Functional Test
SLS Heat Traced Piping and Storage Tank Heater
Operability Test
Daily Checks Logs
Pre-calibrate new [SLS system] relief valve to be
installed in RF-05
Pre-calibrate new [SLS system] relief valve to be
installed in RF-05
Tube Leak in Emergency Condenser
[EC] ¹122, Cut
Inlet/Outlet Piping and Eddy Current Testing
Remove and Evaluate Flow Indications in the Supply
Side of the Tubesheet for HTX-60-42
Tube Leak in ¹111 EC, Cut Inlet/Outlet Piping and
Hemihead
Tube Leak in ¹112 EC, Cut Inlet/Outlet Piping and
Hemihead
M1,2
Re airs to NMP1 Emer enc
Coolin
Condensers
a.
Ins ection Sco
e
The inspectors monitored maintenance
activities to repair the four NMP1 EC
condensers.
The inspectors reviewed WOs and associated
documentation,
monitored personnel to verify adherence to foreign material exclusion (FME)
controls, and discussed the work with maintenance
and radiation protection (RP)
personnel,
and quality assurance
(QA) observers.
0
b.
Observations
and Findin s
The inspectors observed NMP1 maintenance activities related to inspection and
repair of the EC condensers.
The inspectors noted that maintenance
and RP
personnel adhered to posted FME requirements; i.e., personnel were appropriately
logging material into and out-of the FME area, using the Material Accountability Log.
Additionally, the FME for cutting evolutions was controlled, in that weld cuts were
enclosed (i.e., taped over) when work was secured.
The inspectors noted that maintenance
personnel were adhering to the WO
requirements and all associated
procedures
and documentation were readily
available and current.
Hot-work permits were posted at the work site and were
updated daily. Radiological controls within the work area were generally
satisfactory; however, the inspectors noted some air lines running across the
contamination area boundary that were not properly secured
(taped down).
RP personnel were informed and the lines were subsequently secured.
The inspectors discussed
ongoing activities with members of the QA staff.
The
inspectors determined that QA coverage of the EC condenser work was appropriate.
QA personnel were monitoring work activities during dayshift and backshift hours.
During observations,
both the NRC inspectors and QA staff noted a poor work
practice during a pipe cutting evolution. Specifically, maintenance
personnel were
observed removing metal debris and burrs using a rubber-gloved hand while the
cutting machine was in operation.
The inspectors considered this practice both a
safety concern, in that the rubber glove could potentially become entangled
in the
cutting machine and result in personnel injury, and a radiological concern, in that
using a rubber glove to remove metal shavings could potentially result in glove tears
and personnel contamination.
The work supervisor was informed of the concern
and maintenance
personnel were immediately instructed on alternate methods for
removing the material.
C.
Conclusions
During EC condenser repair activities, FME controls were appropriately maintained,
in that material accountability was maintained and system cleanliness was
controlled.
Maintenance personnel adhered to WO requirements
and all associated
procedures
and documentation were readily available and of the current revision.
During a pipe cutting evolution, a poor safety and radiological work practice was
identified, in that maintenance
personnel were using a rubber-gloved hand to
remove metal shavings.
Radiological controls were satisfactory.
QA oversight of
ongoing maintenance
activities was appropriate.
10
M1.3
NMP2 Maintenance Activities on Offsite Power Su
I
On September 30, 1997, NMP2 de-energized
Line 6 and reserve transformer "B" for
planned maintenance.
Line 6 is one of the two TS required 115 kV (kiloVolt)offsite
power supplies from the Scriba switchyard.
10 CFR 50.65 ("The Maintenance
Rule" ) requires an assessment
be made of all plant equipment that is out of service.
This assessment
is to determine the overall effect on the performance of safety
functions, and is to include equipment removed from service for preventive
maintenance activities.
To fulfillthis requirement, NMPC completed
a probabilistic
risk assessment
(PRA) of the planned maintenance activities and concluded that the
overall change in risk was small, and that the expected duration of the outage was
short enough such that the proposed activity did not represent
a significant risk
increase.
The inspectors reviewed the PRA and determined that it accurately
accounted for all equipment out of service at the time of the maintenance,
and
provided a thorough evaluation justifying the conclusion.
The work, including
approximately 48 previously deferred preventive maintenance items, was completed
on October 1, without incident.
Quality Assurance ln Maintenance Activities (61726)
M7.1
Missed Surveillance Test of the NMP1 Control Room Ventilation Radiation Monitor
a.
Ins ection Sco
e
The inspectors reviewed the failure of NMP1 to perform a TS-required surveillance
test within required periodicity, and discussed the event with the NMP1 RP
Manager.
b.
Observations
and Findin s
On August 18, a NMP1 RP calibration technician was preparing to perform a
quarterly instrument channel test for channel ¹11 of the control room (CR)
ventilation radiation monitor. While preparing for the work, the technician identified
that the instrument channel calibration for channel ¹11 had not been performed
within the required periodicity. Specifically, NMP1 TS, Table 4.2.6.I, requires the
instrument channel calibration to be performed once each operating cycle, not to
exceed 24 months.
Channel ¹11 CR ventilation radiation monitor was last
calibrated on August 3, 1995.
Channel ¹11 was declared inoperable on August 18, calibrated and returned to an
operable condition on August 20. The licensee identified the apparent root cause as
inattention-to-detail and failure to self-check the completed preventive maintenance/
surveillance test (PM/ST) data-sheet following completion of the channel ¹12
calibration on April 24, 1996. The PM/ST sheet used during this calibration was
erroneously updated as channel ¹11 by an RP technician and was subsequently
reviewed by supervision.
This information was entered in the PM/ST database,
which reset the 24-month instrument channel calibration clock for channel ¹11; the
actual due date of August 3, 1997, was canceled.
11
The NMP1 RP Manager informed the inspectors that a review of the RP Calibration
History Records and control room logs indicated that the channel ¹12 CR ventilation
radiation monitor instrument channel calibration had been satisfactorily completed
on April 24, 1996, and an instrument channel test and calibration were completed
in July 1997.
Thus, channel ¹12 was always operable and the TS-required
minimum number of channels had always been available.
The inspectors considered the licensee root cause determination to be reasonable.
The failure to complete the TS-required surv'eillance test for channel ¹11 CR
ventilation radiation monitor is a violation of NMP1 TS, Section 4.6.2.a, requiring
sensors
and instrument channels to be checked, tested and calibrated at least as
frequently as listed in Tables 4.6.2.a to 4.6.2.I.
(VIO 50-220/97-07-02) This
violation is not being considered
as non-cited because
missed surveillances have
been a repetitive problem.
C.
Conclusions
Inattention-to-detail and failure to self-check a completed PM/ST data sheet by
NMP1 RP calibration staff resulted in the failure to perform a ventilation radiation
monitor instrument channel calibration within the TS-required periodicity.
M8
Miscellaneous Maintenance Issues (90712, 92700, 92902)
M8.1
Closed
URI 50-220 96-07-04: Procedure
Chan
e Evaluation Used to Chan
e
Intent of a NMP1 Procedure
a.
Ins ection Sco
e
During the NRC IPAP team inspection, it was noted that temporary changes were
made to a surveillance test procedure which appeared to change the intent of the
procedure.
The inspectors reviewed the affected procedure, the procedure change
evaluation, and the associated
DER.
b.
Observations
and Findin s
During the NRC IPAP team inspection, it was noted than temporary changes were
made to an NMP1 surveillance test procedure (N1-ST-Q18, "Core Spray Loop 12
Pump and Valve Operability Test," Revision 4) that appeared to change the intent of
the procedure.
Changing procedure intent as a temporary change is not consistent
with the requirements of the NMP1 TS, Section 6.8.3.
At Nine Mile Point, temporary changes to procedures
are processed
in accordance
with Procedure
NIP-PRO-04, "Procedure Change Evaluations" (PCEs).
As
documented
in the DER (1-96-0822) disposition, NMPC determined that the PCE did
not change the intent of the procedure; although they did identify several
weaknesses
in the administrative processing of the PCEs.
The inspectors reviewed
12
the DER, the PCEs, and the respective safety evaluations,
and determined that the
NMPC conclusion was reasonable.
There was no violation of the TS.
c.
Conclusion
NMPC's implementation of a temporary change to a NMP1 surveillance test
procedure was acceptable,
although weaknesses
were identified by NMPC in the
administrative processing of the PCE.
M8.2
Closed
LER 50-410 97-06: Plant Shutdown Due to Risin
Unidentified Leaka
e
The event described
in this Licensee Event Report (LER) was discussed
in NRC IR
50-410/97-06,Section
02.1.
The description and analysis of the event, as
contained in the LER, were consistent with the inspectors'nderstanding
of the
event.
This LER is closed.
M8.3
Closed
LER 50-410 97-07: Failure to Calibrate H dro en Recombiner Instruments
as Re uired b
Technical S ecifications Due to Procedure Omission
a.
Ins ection Sco
e
NMP2 identified that several instruments in the hydrogen recombiner system (HCS)
had not been calibrated as required by TSs.
NMPC identified this as part of their
review in response to Generic Letter (GL) 96-01. The inspectors reviewed the event
notification, the LER, and the revised surveillance test procedures.
b.
Observations
and Findin s
On August 13, 1997, NMP2 instrumentation and control (IRC) technicians identified
that eight instruments in the HCS were not calibrated during the performance of
surveillance test procedure N2-ISP-HCS-R110, "Operating Cycle Channel Calibration
of the Recombiner Reactor Temperature Instrumentation," Revision 2.
NMP2 TS
surveillance requirement (SR) 4.6.6.1.b.1 requires a channel calibration at least
every 18 months.
The IRC technicians identified this while reviewing the
procedure,
in accordance with the NMPC response to GL 96-01, "Testing of Safety-
Related Logic Circuits." The missed calibrations were documented
on DER 2-97-
2395.
Since both trains of HCS were affected, the limiting condition for operation (LCO) in
TS Section 3.0.3 was applicable.
TS LCO 3.0.3 would require the reactor be
shutdown within twelve hours; however, TSSR4.0.3 allows up to 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> for
completion of the surveillance.
NMPC processed
a procedure change to incorporate
the calibration of the missed instruments into N2-ISP-HCS-R110; after which,
Division I HCS was satisfactorily calibrated, and returned to service.
Shortly
thereafter, Division II was tested and declared operable.
In the LER, the root cause was identified as inadequate communication during initial
procedure development.
Also, a contributing cause was noted as poor work
13
practice during subsequent
revision of the procedure.
As one of the corrective
actions, NMPC stated that NMP2 willcontinue to review the logic circuits to ensure
that surveillance test procedures
are consistent with TS requirements.
In addition,
administrative procedures related to procedure reviews were revised to add
assurance
that procedures were technically adequate.
Notwithstanding, NMP2
violated TSSR 4.6.6.1.b.1, which requires a channel calibration of all HCS
instrumentation at least once every 18 months.
(VIO 5041 0/97-07-03) This
violation is not being considered
as non-cited because
missed surveillances have
been
a repetitive problem.
The inspectors reviewed the LER and found it to be timely and to accurately
describe the event.
The immediate corrective actions and actions to prevent
recurrence were appropriate.
This LER is closed.
c.
Conclusion
The inspectors considered the discovery by the NMP2 ISC technicians of the
missing calibrations in the HCS to be good.
However, NMPC continues to have
instances of missed TS surveillances,
as noted in this and previous inspection
reports.
III. ENGINEERING
E1
Conduct of Engineering (37551)
E1.1
General Comments
Using NRC Inspection Procedure 37551, the resident inspectors frequently reviewed
design and system engineering activities, including justifications for operability
determinations,
and the support by the engineering organizations to plant activities.
Specialist inspectors in this area used other procedures
during their reviews of
engineering activities; these inspection procedures
are listed, as applicable, for the
respective sections of the inspection report.
E8
Miscellaneous Engineering Issues (90712, 92700, 93903)
E8.1
Closed
Desi n Control Measures
Inade
uate durin
Calculations for Establishin
Reactor Buildin
and Turbine Buildin
Relief Pressure
The inspectors verified implementation of the corrective actions specified in the
licensee's response,
dated July 16, 1996, to the notice of violation. The actions
taken by NMPC to preclude a recurrence of design control inadequacies
included:
An independent review of a sample of 29 NMP1 structural engineering
calculations (that were originally performed by the engineer who incorrectly
calculated the initial blowout panel relief pressure) was completed in April
14
1996.
The independent reviewer, a NMP2 structural engineering supervisor,
found no similar technical errors.
The NMP1 engineering branch manager and structural engineering supervisor
emphasized to the structural group the importance of understanding the
function and behavior of a structural element before performing a calculation,
understanding the differences in the mathematical assumptions when
designing a component to fail rather than to provide structural support, and
in providing a clear and self-explanatory conclusion in the end of calculations
that does not require further interpretation of results.
~
A lessons learned transmittal was disseminated to other organizations to
communicate the facts and root cause surrounding the calculational error.
~
The engineers
and designers
in the structural group were retrained on
Procedure
NEP-DES-OB, "Calculations," to properly understand the role of a
preparer, checker, and approver related to a calculation.
~
The engineering branch revised the guideline used to perform a DER
Operability Supporting Analysis (NEG-1E-006) to emphasize the role of a
supervisor in checking the DER disposition with the results of the calculation,
particularly those associated with operability determinations and the potential
for reportability.
The inspectors reviewed the relevant documentation supporting completion of these
corrective actions and concluded that the actions taken were those as described in
the licensee's July 16, 1996 response.
This item is closed.
E8.2
Closed
URI 50-220 96-05-01: NRC Staff Review of Revised Reactor Buildin
and
Turbine Buildin
Blowout Panel Relief Pressure
Calculations
LER 50-220/95-05identified the existence of an initial construction deficiency and a
subsequent
1993 design calculation error associated with the reactor building (RB)
and turbine building (TB) blowout panels.
An enforcement conference was held
regarding this matter on April 12, 1996; a Notice of Violation (Severity Level III) and
Civil Penalty were issued on June 18, 1996.
In response to the event, NMPC
reanalyzed the upper bound pressure relief capacities of the RB and TB blowout
panels and the lower bound structural failure capacities of the buildings to
demonstrate that the panels would fail due to internal pressure prior to failure of the
buildings. This would achieve the intended pressure relief function, as stipulated in
In reviewing the NMPC response,
the inspectors requested
assistance
from the NRC Office of Nuclear Reactor Regulation (NRR) to determine
the technical adequacy of the revised design calculations for the RB and TB blowout
panels.
On August 20, 1996, staff from the NRR Division of Engineering conducted
an audit
of the revised design calculations and performed a walkdown of the RB and TB
blowout panels.
This led to identification of additional items requiring licensee
V
response
and resolution.
In reviewing the NMPC calculations to support the re-
analysis, the NRC staff identified several errors.
Deficiencies included that the
structural dead load was not independently treated in computing the structural
failure capacity, and a high strain rate factor was inappropriately used in
determining RB and TB pressure capacity.
However, the staff judged the safety
consequence
of the errors to be low, since the correction of the errors would not
have appreciably affected the computed structural capacities or changed the
conclusion.
Subsequently
on November 15, 1996, NMPC submitted revised calculations.
The
NRR staff reviewed the licensee's submittal, and concluded that the panels would
perform their intended pressure relief safety function in a manner consistent with
the applicable licensing basis, as stated in the NMP1 UFSAR. The revised
calculations determined that the blowout panel upper bound pressure for the RB
was 65 pounds per square foot (psf), and for the TB was 62 psf. The recalculated
ultimate lower bound superstructure
capacities were 117 psf and 135 psf for the RB
and TB, respectively.
This showed that there was ample safety margin for pressure
relief of the buildings.
In addition, a concern was expressed
by the NRC staff during the enforcement
conference regarding the safety of the condensate
storage tanks housed in the TB,
in the event that a falling RB blowout panel impacted the TB roof. NMPC provided
calculations to demonstrate the structural integrity of the TB roof and to assure the
safety of the condensate
storage tanks.
The calculations provided for NRC review
were initiallyfound to be technically deficient with respect to the proper
assumptions for calculating the kinetic energy of a faIling panel.
NMPC submitted
revised calculations, which the staff found acceptable.
The results showed that the
safety of the condensate
storage tanks was not compromised, since the roof was
capable of absorbing the energy of a falling panel without rupturing or experiencing
large deformation.
Therefore, the safety consequence
of the errors was low.
The errors identified by the NRC indicated that the licensee's design control
measures,
in place prior to the NRC audit of August 20, 1996, were not fully
effective in assuring the accuracy of the revised calculations regarding this matter.
However, based on the low safety significance of the errors identified, and NMPC's
correction of the errors, this constitutes
a violation of minor significance, and is
being treated as a Non-Cited Violation, consistent with Section IV of the
(NCV 50-220/97-07-04)
Closed
IFI 50-220 96-05-02: Inconsistencies
in the NMP1 UFSAR and IPE with
res ect to the Reactor Buildin
and Turbine Buildin
Blowout Panel Relief Pressure
~Set oints
NMPC identified discrepancies
between the'various sections of the UFSAR regarding
the stated value of the pressure relief capacity of the RB and TB blowout panels.
In
reviewing the associated
event, the NRC identified similar inconsistencies within the
Individual Plant Examination (IPE) with respect to blowout panel relief pressure.
16
A Licensing Document Change Request (LDCR 1-96-UFS-035), with the supporting
10 CFR 50.59 Safety Evaluation (No.96-021), was approved by NMPC to revise
the RB and TB blowout panel relief pressure setpoints,
as described in the UFSAR.
The relevant tables and sections of the UFSAR have been revised to change the
failure load of the RB and TB blowout panels to 65 psf and 62 psf, respectively.
Also, the relevant UFSAR sections were revised to change the failure loads of the
to 117 psf and 135 psf, respectively.
In support of the UFSAR changes,
NMPC performed an evaluation to determine if an
unreviewed-safety-question
existed for the corrected parameters.
An evaluation of
the equipment qualification (EQ) analysis, using the revised relief pressures,
was
also
performed to determine if there was an increase
in the probability of equipment
malfunction.
It was concluded by the NMPC staff that equipment in the RB and TB
would remain qualified following the maximum temperature,
pressure,
and humidity
resulting from a high energy line break.
Through NMPC's Fuels and Analysis Group, the inconsistencies
blowout panel relief pressures
were evaluated to determine if the IPE results were
affected by the revised values.
Using a Modular Accident Analysis Program, the
blowout panel relief setpoint was varied from 0.01 psf (assumed to open early) to
infinite psf (assumed
never to open).
The results indicated that the IPE results were
not significantly changed due to other existing leakpaths and the postulated failure
of building ventilation systems.
The inspectors concluded that the licensee has taken the appropriate actions to
remove inconsistencies
regarding RB and TB blowout panel relief pressures
as
stated in the UFSAR and IPE. An evaluation using the revised parameters for EQ
analyses
has shown the results to be consistent.
The inspector had no further
questions.
E8.4
Closed
LER 50-220 97-07: Potential Control Room Emer enc
Ventilation S stem
0 eration Outside the Desi
n Basis due to Inade
uate Evaluation
ae
Ins ection Sco
e
The inspectors reviewed the DER and LER associated with the NMP1 control room
smoke purge system impact on the operability of the control room emergency
ventilation system.
The inspectors discussed the issue with a NMP1 SSS and the
NMP1 Plant Manager.
b.
Observations
and Findin s
On August 6, 1997, a NMP1 operator questioned the ability of the control room
emergency ventilation system (CREVS) to fulfillits accident mitigation function with
the control room smoke purge system (CRSPS) in operation.
Specifically, if a high
radiation signal resulted in an automatic initiation of the CREVS, and the CRSPS was
already in operation, the design function the CREVS to maintain control room air
quality would have been inhibited.
Outside air would continue to enter the control
17
room until the CRSPS was manually secured, since the CRSPS did not have an
automatic isolation feature.
The inspectors considered the questioning attitude of
the operator to be very good.
The licensee subsequently
issued
DER 1-97-2326 to
address the concern.
On August 15, following an engineering evaluation, the
licensee reported this issue to the NRC, in accordance with 10 CFR 50.72.
The CRSPS was designed to clear the smoke and maintain a habitable atmosphere
in the control room and auxiliary control room (i.e., relay room) in case of a fire.
However, the licensee also used the system during periods when the normal control
room ventilation was secured for maintenance.
The LER stated additionally that the
CRSPS had been operated at times other than its intended design and concurrently
when CREVS operability was required.
The inspectors reviewed the LER and found that it accurately described the event.
Licensee immediate corrective actions included placing administrative controls on
the CRSPS control switch to prevent operation without first considering the
potential impact on operability of the CREVS.
Long-term corrective actions were to
revise operating and test procedures for the CRSPS to ensure the system is
operated only for smoke removal, and to ensure that the system is tested only when
the CREVS is not required to be operable.
Additionally, the licensee planned to
review selected modifications performed in the 1980s for similar system interface
deficiencies.
The inspectors considered both the immediate and long-term
corrective actions to be appropriate.
The licensee root cause evaluation attributed the deficiency to an inadequate
evaluation of the CRSPS interface with the CREVS during modifications in.1980 and
in 1984. This is a violation of 10 CFR 50 Appendix B, "Quality Assurance Criteria
for Nuclear Power Plants and Fuel Reprocessing
Plants," Criterion III, "Design
Control." This licensee-identified and corrected violation is being treated as a Non-
Cited Violation, consistent with Section VII.B.3 of the NRC Enforcement Policy.
(NCV 50-220/97-07-05)
c.
Conclusions
An NMP1 operator's questioning attitude of the control room smoke purge system
was very good and resulted in an engineering operability evaluation of the impact on
CREVS operability. Notwithstanding, the interface between the smoke purge
system and CREVS was inadequately evaluated during modifications in the early
1980s.
IV. PLANT SUPPORT
Using NRC Inspection Procedure 71750, the resident inspectors routinely monitored
the performance of activities related to the areas of radiological controls, chemistry,
security, and fire protection.
Minor deficiencies were
discussed with the appropriate management,
significant observations
are detailed
below.
Specialist inspectors in the same areas used other procedures during their
I
18
reviews of plant support activities; these inspection procedures
are listed, as
applicable, for the respective sections of the inspection report.
R1
Radiological Protection and Chemistry (RP&C) Controls (71750, 83750, 86750,
R1.1
General Comments
During entry into and exit from radiologically controlled areas (RCAs), the inspectors
verified that proper warning signs were posted, personnel entering were wearing
proper dosimetry, personnel and materials leaving were properly monitored for
radioactive contamination, and monitoring instruments were functional and in
calibration.
During periodic plant tours, the inspectors verified that radiation work
permits (RWPs) and survey maps were current, and that they accurately reflected
plant conditions.
They observed activities in the RCAs and verified that personnel
were complying with the requirements of applicable RWPs, and that workers were
aware of the radiological conditions in the area.
R1.2
Radiolo ical Protection Pro ram
a.
Ins ection Sco
e
The inspectors reviewed the ALARA(as-low-as-is-reasonably-achievable)
post-
outage job reviews, personnel contamination reports, selected exposure evaluation
reports (EERs), and a vendor audit, under the National Voluntary Laboratory
Accreditation Program (NVLAP). In addition, the inspectors conducted tours
(including NMP2 lower reactor building rounds with a plant operator); and
interviewed station staff.
b.
Observations
and Findin s
Work scope additions to the extended
NMP1 fourteenth refueling outage (RFO14)
were responsible for the RFO14 ALARAgoal being exceeded.
The ALARAgoal was
set at 276 person-rem, actual exposure accrued was about 299 person-rem.
Major
work scope additions included inspection of five recirculation system welds, repair
of four valves after local-leak-rate-testing
failures, rolling four stub tubes under-
vessel, and additional core shroud inspections and tie-rod repairs.
This additional
work accounted for 36.2 person-rem,
and minor tasks contributed an additional
13.5 person-rem.
The licensee had budgeted
15 person-rem for emergent work.
Another important contributor to exceeding the original goal was that the work
scope increase extended the outage from a planned 35 days to 67 days.
Exposure
for the NMP2 RFO5 was less than the ALARAgoal.
The ALARAgoal was set at
215 person-rem, actual exposure was 182 person-rem.
The inspectors noted that
lessons learned in conducting work at both units had been captured for future
consideration.
No contamination events of regulatory concern were noted.
The
inspector assessed
that postings and labels were established
in accordance with the
licensee's program.
Thermoluminescent dosimeter (TLD) services were vendor-supplied; the vendor was
NVLAP approved, as required.
The inspectors reviewed the most recent NVLAP
assessment
of the vendor laboratory and discussed
the vendor's actions pertaining
to deficiencies and comments.
The Dosimetry Supervisor continued to oversee the
adequacy of the program.
No inadequacies
were noted in any of the EERs
reviewed.
As noted during tours, individuals were wearing the required dosimeters.
The inspectors noted that no contaminated
area entries were required of the NMP2
operator during the conduct of rounds in the lower reactor building. Also, the plant
operator had to make few high radiation area (HRA) entries, as the licensee had
installed cameras
in many HRAs, allowing the operators to take readings while
remaining outside the cubicles.
Very good radiological housekeeping
was noted in
NMP2.
Conclusions
The radiological protection program area was being well-implemented.
The NMP1
outage ALARAgoal was exceeded
due to emergent work. Very good radiological
housekeeping
was noted in NMP2. Effective programs were implemented for
contamination control and external dosimetry.
Trans ortation and Radiolo ical Waste Pro rams
Ins ection Sco
e
The inspectors reviewed the licensee's programs for the processing of liquid and
solid radiological waste (radwaste) and the transportation of radioactive materials,
including: the Process Control Program (PCP), shipping records, scaling factor data
(for compliance with 10 CFR 61.55), and system walkdowns in radwaste.
Observations
and Findin s
The NMP1 radwaste processing program was described
in the NMP1 radwaste
Process Control Program, Revision 2, dated November 15, 1994.
The inspectors
noted that the NMP1 PCP lacked any specifics on the way the unit processed
wastes, and that it contained erroneous references to federal regulations,
specifically outdated versions of 10 CFR 20 (significantly revised in 1994) and 49
CFR (revised in 1996).
Failure to incorporate into the PCP the changes
in 10 CFR 20 and 49 CFR indicate that the PCP was not periodically reviewed and revised.
Failure to maintain the PCP is an apparent violation of NMP1 TS 6.8, which requires
that procedures specified in Regulatory Guide 1.33 be written, maintained and
adhered to for plant operations.
Regulatory Guide 1.33 includes procedures for the
processing of liquid and solid radwaste, for which the PCP is the core document.
(EEI 50-220/97-07-06)
20
The inspectors reviewed the shipping records for five shipments of radwaste and
radioactive material
~
In general, the documentation for shipping radioactive material
and radwaste was clear and complete and in accordance with 10 CFR and 49 CFR.
However, one of the shipments reviewed was noted not to be in compliance with
regulations.
On July 24, 1997, the licensee shipped two metal samples from the
core shroud to BWX Technologies,
Inc. Upon receipt, it was noted by BWX that
radiation levels in an occupied portion of the vehicle were 2.8 milliRem per hour
(mRem/hr), in excess of the regulatory limit of 2 mRem/hr, as specified in 49 CFR
173.441; this is an apparent violation.
(EEI 50-220/97-07-07)
The inspectors toured portions of the radwaste systems located in various buildings,
All facilities were found to be generally neat and orderly, and the conditions in these
facilities had noticeably improved during the past three years.
The inspectors noted,
however, that the ¹11 concentrated
waste tank still had concentrates
in it, even
though the ¹11 waste evaporator was taken out of service over 17 years ago.
The
NMP1 UFSAR for the tanks and vessels
in the radwaste system assumes that the
tanks regularly receive and discharge waste materials.
No analysis was performed
for wastes being indefinitely stored in one of the tanks.
The inspectors discussed
with the licensee the fact that the conditions in ¹11 concentrates
tank are not
described or analyzed in the UFSAR. The licensee agreed to conduct a detailed
evaluation and provide to the NRC the results of their review, including a plan of
action for ensuring the safe use of concentrates tank ¹11 or the removal of the tank
contents..
(IFI 50-220/97-07-08)
The inspectors also reviewed the NMP1 UFSAR, specifically Sections 11.2 (liquid
waste) and 11.3 (solid waste) and compared the systems and process descriptions
with current plant operations.
The inspectors determined that both sections were
significantly out-of-date and required revision.
The licensee provided documentation
that indicated that such a revision was currently underway for the UFSAR in
general, and that Sections 11.2 and 11.3 were included in this revision,
NMP2
The inspectors reviewed the licensee's
program for radwaste processing,
as
described
in the NMP2 radwaste Process Control Program, Revision 2, dated
November 15, 1994.
The inspectors identified that within this document,
references to 49 CFR were out of date, following the revisions to 49 CFR in April
1996.
Failure to maintain the PCP, is an apparent violation of Technical Specification 6.13.
(EEI 50-410/97;07-06)
The inspectors reviewed shipping records for radwaste and radioactive material
transportation.
All records reviewed were in compliance with regulations contained
in 10 CFR Parts 20, 61 and 71, and 49 CFR Parts 170-177.
The records reviewed
were clear and concise, and included documentation related to shipping manifests,
shipment classification, waste classification (where applicable), and emergency
notifications.
21
The inspectors toured the NMP2 radwaste facilities, and found them to be well
maintained, appropriately posted, and with only small areas kept as contaminated.
The inspectors also reviewed the NMP2 UFSAR and determined that Section 11.2
(liquid radwaste) and 11.4 (solid radwaste) had only minor discrepancies
relative to
current plant operations.
The licensee provided documentation indicating that
revisions to the UFSAR which willaddress the discrepancies
have already been
drafted.
Common
The inspectors reviewed the licensee's program for determining hard-to-measure
radionuclides, in order to comply with 10 CFR 61.55.
The licensee periodically
submitted waste stream samples to a vendor laboratory for total isotopic analysis,
and derived waste stream specific scaling factors from the results.
The inspector
reviewed the licensee's program for ensuring the applicability of the scaling factors,
and determined that the licensee's procedures
in support of this program were
vague.
The licensee agreed with the inspectors'bservations
and indicated that a
review of these procedures would be conducted to determine what additional
guidance would be appropriate.
c.
Conclusions
A generally effective radwaste program'had been established
at each unit; but
procedures
and associated
documentation
(PCP and UFSAR) have not been properly
maintained.
(EEI)
In addition, one shipment of radioactive material resulted in the
occupied portion of the vehicle exceeding allowed limits.
(EEI) Plant conditions
were generally very good relative to radiological housekeeping
in radwaste.
However, the lay-up of waste concentrates tank ¹11 at NMP1 is questionable;
NMPC stated that a written plan of action for dealing with it would be provided to
the NRC.
(IFI)
R1.4
Shi ment of Radioactive Material to an Unlicensed Facilit
a.
Ins ection Sco
e
The inspectors discussed the circumstances
surrounding a radioactive material
shipment to an unlicensed facility with the NMP1 radwaste supervisor and NMP2 RP
Manager.
b.
Observations
and Findin s
On September 25, 1997, a metal sample removed from a NMP1 EC condenser tube
sheet was shipped to BWX Technologies, Inc., in Lynchburg, Virginia, for laboratory
analysis.
This sample was prepared for shipment as a "limited quantity" in
accordance with 49 CFR 173.421.
A limited quantity is defined as the maximum
amount of a hazardous material for which there is a specific labeling or packaging
exception.
0
22
The radwaste supervisor informed the inspectors that the manifest had been
properly prepared and was properly addressed.
The package was sent to the
licensee's warehouse for shipment by common carrier.
Warehouse staff placed the
shipping label used by the common carrier (with the incorrect address)
over the
correct shipping address originally placed on the package.
The incorrect address
resulted in the package being delivered to the BWX Contracts Officer in an
administration office complex, in lieu of the laboratory facility. The shipment arrived
at the office complex on the morning of September 26. The Contracts Officer
realized the shipping error, did not open the package,
and notified NMPC of the
error.
The package was shipped to the laboratory facility on September 29 and
arrived on September 30. The BWX office complex was not specified on the
Material License Certificate for receipt of radioactive shipments.
During the inspection, the inspectors ascertained that on May 24, 1995, a similar
radioactive shipment error occurred.
Specifically, a source range detector was
shipped to the wrong General Electric (GE) location.
The shipment went to GE-San
Jose, California, rather than GE-Twinsburg, Ohio.
GE-San Jose did not have a
license to receive radioactive material.
GE informed NMPC, and the shipment was
redirected to the GE-Twinsburg facility in Ohio. As in the September 1997 event,
the manifests had been properly prepared, but warehouse
personnel sent the
package to the wrong address.
The inspectors discussed
both events with the NMP1 RP Manager.
The RP Manager
indicated that Nuclear Procurement Administrative Procedure NPAP-INV-210,
"Receipt, Test, Inspection and Processing of Materials, Parts and Services,"
Revision 8, defined the requirements for material shipments offsite.
In response to
the 1995 event, NPAP-INV-210 was changed to incorporate an independent
verification of the required documentation to assure the item was ready for
shipment.
The inspectors considered the corrective actions for the 1995 event to
be ineffective in preventing recurrence.
10 CFR 30.41 requires a licensee transferring radioactive material to verify that the
transferee's
license authorizes the receipt of the type, form, and quantity of
byproduct material to be transferred.
Contrary to the above, on two occasions,
NMPC shipped radioactive material to an unlicensed facility. This is an apparent
violation of NRC regulations.
(EEI 50-220/97-07-09)
c.
Conclusions
On two occasions,
personnel inattention-to-detail and inadequate verification
resulted in the transfer of radioactive material to a location not authorized to receive
such material.
Furthermore, the corrective actions for the first event were
ineffective in preventing recurrence.
(EEI)
23
R2
Status of RP&C Facilities and Equipment (83750)
R2.1
Radiolo ical Protection Facilities and Contamination Controls Instrumentation
a.
Ins ection Sco
e
The inspectors reviewed licensee changes to RCA access controls and the manner
in which contamination controls instrumentation had been calibrated.
b.
Observations
The inspectors noted that the licensee had assessed
the impact of the recent
10 CFR 61 scaling factors on the instrumentation program.
Radioisotopes chosen
for frisker (Eberline RM-14) source checks and calibrations were appropriate, based
on the licensee's
10 CFR 61 assessment.
The inspectors considered the licensee's
efforts in upgrading their small article monitors (SAM) to the equivalent of SAM
Model-9 to be a good initiative. The inspectors reviewed the SAM alarm set points
at NMP2 and found them appropriate.
Since the last inspection of this area, the licensee improved the RCA access point
by installing turnstiles.
This should help to ensure that workers have the correct
dosimetry to comply with the appropriate radiation work permit.
Bar codes have
been relocated from security badges to TLDs and the RCA turnstiles are unlocked by
inserting an operating electronic dosimeter into the turnstile resulting in computer
logging of an RCA entry.
This area was being well-implemented.
Installation of additional access control
devices has improved this program area.
R3
PR&C Procedures
and Documentation (71750)
, R3.1
Shi ment of Wron
Radwaste Material
a.
Ins ection Sco
e
NMPC personnel loaded and shipped an incorrect liner of low-level radwaste to a
facilityfor disposal.
The inspectors interviewed the personnel involved and their
management,
and reviewed the associated
procedures
and documentation.
b.
Observations
and Findin s
On September 5, 1997, NMPC informed the resident inspectors that an incorrect
liner of low-level radwaste was shipped for disposal.
During the unloading of the
liner, the recipient, Molten Metal Technology, noted that radiation levels in the area
of the liner were higher than expected.
24
During their investigation, NMPC discovered that on September 3, an NMP1
radwaste operator inadvertently loaded the wrong liner, consisting of dewatered
resin and charcoal filter material from NMP2, into the shipping cask for transport to
Molten Metal Technology.
The liner that was supposed to have been shipped was
filled in 1995, the liner that was actually shipped was filled in 1997.
The NMP1
radwaste facility is used for interim storage of all radioactive material awaiting
shipment from NMP. The radwaste shipment schedule had the wrong location for
the liner. Although each liner has a unique identffication number, the radwaste
operator failed to check the number on the liner with the number on the shipment
schedule,
using only the storage location number.
Before the truck left the NMP1 radwaste facility, an NMP1 radiation protection (RP)
technician conducted
a radiation survey of the cask and sent the results to the
NMP2 RP technician who authorized the shipment and signed the associated
shipping manifest.
The NMP2 RP technician did not review the radiation survey; if
he had, he would have noted that the radiation levels on the surface of the liner
were almost four-times those expected.
Readings for the 1995 liner were expected
to be about 800 milliRem per hour (mRem/hr); the actual survey showed 3,000
mRem/hr on contact with the liner.
The inspectors discussed the event with the Radwaste Supervisors for both units,
and reviewed the associated
documentation.
The discussions with the supervisors
confirmed that there were missed opportunities for the identification that the wrong
liner had been loaded.
In addition, the inspectors determined that there were no
procedures directly related to the loading of liners or the shipment of radwaste
material.
Immediate corrective actions included a requirement for plant manager
approval of all radwaste shipments.
10 CFR 20, Appendix G, "Requirements for Transfers of Low-Level Radioactive
Waste Intended for Disposal at Licensed Land Disposal Facilities and Manifests,"
Section I.B, requires the shipper [NMPC] of radioactive waste to provide information
regarding the shipment on the manifest, including the total radionuclide activity in
the shipment.
10 CFR 71, "Packaging and Transportation of Radioactive IVlaterial,"
Paragraph 71.5, requires each licensee [NMPC] who delivers licensed material to a
carrier for transport to comply with the requirements of 49 CFR 172. 49 CFR 172,
Paragraph
172.203, requires for shipments of Class 7 (radioactive) material to
include the activity contained in each package of the shipment.
Contrary to the
above, the shipping manifest did not accurately reflect the actual radionuclide
activity of the shipment; this is an apparent violation of 10 CFR 20 and 49 CFR
172.
(EEI 50-220/97-07-10& 50-410/97-07-10)
Conclusion
NMPC personnel loaded and shipped the wrong liner of low-level radwaste to a
facility for disposal.
(EEI)
In less than two months, three different shipments from
the Nine Mile site were inadequately controlled (also see Sections R1.3 and R
1 4 of
this report).
AII three appear to be due to a combination of a lack of procedures
25
describing shipping activities, inattention-to-detail on the part of the radwaste
operators,
and a lack of supervisory oversight.
R5
Staff Training and Qualifications (86750, Tl 2515/133)
R5.1
Trainin
of Staff Involved in Radioactive Material Trans ortation and Radwaste
~Processin
a.
Ins ection Sco
e
The inspectors reviewed the licensee's program for the training of personnel
involved with radwaste processing and radioactive material transportation.
b.
Observations
and Findin s
The licensee has established two distinct training programs for plant workers
involved in transportation and radwaste processing.
One program was presented to
workers involved in waste certification and shipping, in accordance with NRC
Inspection and Enforcement (IE) Bulletin.79-19. The second program was for
workers involved in the receipt or shipment of radioactive materials, in accordance
with 49 CFR 172.700.
This second program used
a tiered approach to training,
involving lesson plans of increasing difficulty, with the highest level of training given
to the workers who certify shipments.
For 1996, the lic'ensee sent a number of plant personnel to a vendor training
program to meet its IE Bulletin commitment and to satisfy the requirements of
49 CFR. This training was reviewed in advance by the Nine Mile Point training
department.
Appropriate documentation was contained in the training records for
the inspectors to determine that the vendor training was the equivalent of the
licensee's program.
C.
Conclusions
The licensee has established
a good and well documented training program for
workers involved in radwaste processing
and the shipment of radioactive materials.
R7
Quality Assurance (QA) in RP&C Activities (83750, 86750, TI 2515/133)
R7.1
QA in Radiation Protection Activities
a.
Ins ection Sco
e
The inspection consisted of reviews of DERs; the RP "First Quarter 1997
Radiological Engineering Self Assessment
Report for NMP2," performed in
accordance with "NIP-ECA-05, "Radiation Protection Branch Self-Assessment,
Radiation Worker Practices;" and QA Audit Number 96017, "Radiation Protection
Program."
In addition, the inspectors interviewed the RP managers.
26
Observations
and Findin s
The inspectors noted that RP self-assessments
were a good initiative and a tool for
augmenting QA audits/surveillances.
The assessments
were conducted by RP
department staff and were used to assess
and provide immediate feedback to
station workers on their radiation worker practices.
The department self-
assessments
were objective and self-critical.
A low threshold for RP-related DERs was noted.
A proper level of attention was
. placed on DERs depending on their significance and complexity. Corrective actions
were both timely and reasonable for the DERs reviewed.
The use of subject-matter
expert in the conduct of QA Audit 96017 was considered to be a good initiative.
No items of regulatory significance were noted during the inspectors'eview of the
DERs or the QA audit.
Overall, a very high level of attention has been placed in
improving human performance in the RP area.
C.
Conclusions
Those aspects of the QA program reviewed were well-implemented.
Audits and
self-assessments
were of appropriate scope and technical depth.
R7.2
QA in Radiolo ical Trans ortation and Radwaste Activities
a 0
Ins ection Sco
e
The inspectors reviewed the licensee's program for the assurance
of quality in
waste processing
and transportation of radioactive materials.
The inspectors
evaluated this program through the review of licensee conducted audits and
surveillances.
b.
Observations
and Findin s
NMP1 TS 6.5.3.8 and NMP2 TS 6.5.3.8 require that an audit be conducted every
24 months of the respective unit Process Control Program (PCP).
The inspectors
reviewed the licensee's audit of the PCP (Audit 96002, dated December 19, 1996).
This audit failed to identify out-of-date references to federal regulations contained in
both the NMP1 and NIVIP2 PCPs.
Additionally, while the audit did identify out-of-
date references to training procedures
in the PCPs, the DER issued to identify this
finding was closed without the PCPs being revised to correct the defect.
The
inspectors noted that 10 CFR 50, Appendix B, Criterion XVI, "Corrective Action,"
requires that measures
be established to assure that conditions adverse to quality
are promptly identified and corrected.
The inspectors noted that the failure to
identify conditions adverse to quality, and the failure to ensure that such conditions
are corrected, are apparent violations of 10 CFR, Appendix B, Criterion XVI. (EEI
50-220/97-07-1
1 8( 50-410/97-07-1 1)
The inspectors also reviewed the licensee's program of vendor audits.
The licensee
could only identify one audit of a vendor, Chem Nuclear Systems, qualified to
27
supply NRC-certified shipping casks or waste processing services.
The licensee
does use NRC-certified casks from another vendor, SEG, Inc.; and uses both SEG
and Molten Metal Technologies as waste processors.
No audits of these vendors
were conducted.
Regarding the use of vendor shipping casks, the inspectors noted
that 10 CFR 71.12 allows the NRC to issue a general license to deliver for transport
radioactive material in a package for which the NRC has issued
a certificate of
compliance.
The general license requires that the licensee have in-place a QA
program, approved by the NRC, that satisfies the provisions of 10 CFR 71, Subpart
H (Quality Assurance).
10 CFR 71, Subpart H, requires, in part, that a
comprehensive
system of planned and periodic audits be conducted to verify
compliance with all aspects of the QA program.
The licensee transported
radioactive material in a shipping container owned by SEG, Inc., for which the NRC
has issued a certificate of compliance; however, the licensee had not conducted
periodic audits of SEG to verify compliance with all aspects of the vendors NRC-
approved quality assurance
program.
The inspectors noted that the failure to
conduct audits of suppliers of NRC-certified shipping casks is an apparent violation
of 10 CFR 71.12. (EEI 50-220/97-07-12& 50-410/97-07-12)
Regarding the use of vendor provided radwaste processing systems, the inspectors
noted that NMP1 TS 6.8 requires that procedures
and administrative policies for
activities listed in Appendix "A" of NRC Regulatory Guide (RG) 1.33 be established,
implemented and maintained.
RG 1.33, Appendix "A" lists procedures for the
processing of radioactive waste.
The NMP1 Radwaste
PCP, paragraph 3.1.1,
requires, in part, that radioactive waste may be processed
using approved vendor
equipment and procedures provided that the vendors have a QA program that meets
NRC requirements.
The inspectors noted that the failure to verify the QA program
of radwaste processing vendors is an apparent violation of TS 6.8.
(EEI 50-220/97-07-13)
Conclusion
The QA program failed to identify fullythe defects within the unit specific PCPs,
and in one instance failed to ensure that corrective actions were taken to address
an
identified defect.
(EEI) Additionally, a number of required audits of vendors
providing transportation and/or waste services were not performed.
(EEI)
Conduct of Security and Safeguards Activities (92904, 93702)
General Comments
During routine tours, the inspectors verified that security posts were properly
staffed, protected area gates and vital area access points were locked or guarded,
and isolation zones were free of obstructions.
In general, access controls were in
'ccordance
with the Nine Mile Point Security Plan.
28
S1.2
Unusual Event - Discover
of a Sus
icious Packa
e
a.
Ins ection Sco
e
The discovery of a suspicious looking package inside of the protected area perimeter
resulted in the declaration of an Unusual Event at NMP2.
b.
Observations
and Findin s
On August 18, 1997, a NMP security guard noticed a suspicious looking package
next to the NMP2 maintenance
building. As a precaution, the NMP2 SSS ordered
the maintenance
and operations buildings evacuated.
Shortly thereafter, plant
security personnel examined the package and determined that it was an empty box,
that had apparently blown out of a nearby trash receptacle.
Concurrent with security personnel examining the package, the SSS reviewed the
NMP2 Emergency Plan and procedures.
The SSS declared an Unusual Event, based
on EPIP-EPP-02, Attachment 1, "Emergency Action Level Matrix / NMP2," Revision
6, Category 8.1.1: "Any security event which represents
a potential degradation
in
the level of safety of the plant." After security personnel determined that the
package was not a threat, the SSS terminated the event.
The inspectors considered the response of the security personnel to be acceptable.
The actions by the SSS for the emergency declaration, and termination, were
appropriate and timely. The required notifications to the NRC and state/local officials
were in accordance with the NMPC Emergency Plan.
c.
Conclusion
The response of the Nine Mile Point security personnel to a "suspicious looking"
package was acceptable.
The declaration, by the SSS, of an Unusual Event was
appropriate and in accordance with the NMP2 Emergency Plan.
F2
Status of Fire Protection Facilities and Equipment (71750,92904)
F2.1
Control Room Fire Su
ression S stem and 0 erator Res
onse
a.
Introduction
In response to a recent event at another nuclear power station, the inspectors
reviewed the current fire suppression
systems installed for both NMP1 and NMP2
control rooms.
This included a review of TSs, applicable procedures,
and
surveillance tests.
The inspectors discussed the issues with fire protection
supervisors from both units.
~Back round
On August 7, 1997, an inadvertent actuation of the halon fire suppression
system
occurred in the control room and adjacent central alarm station (CAS) at the
Haddam Neck Nuclear Power Station.
Personnel evacuated
both areas, the control
room was unmanned for about one hour; the licensee declared an Unusual Event.
Just prior to the actuation, personnel were taking photographs of the halon
actuation panel.
Preliminarily, the licensee determined that the inadvertent actuation
was due to the camera flash causing the fire detection system to actuate.
Observations
and Findin s
The inspectors discussed the general area fire suppression
systems for both control
rooms with the Nine Mile Point fire protection supervision.
Neither control room has
an automatic fire suppression
system; they must be manually actuated.
Fire
extinguishers have been staged at several locations within the control rooms, both
carbon dioxide and water types.
Also, several manual hose stations were located
outside each control room.
Both control rooms have general area ionization-type
smoke detectors
in the overhead and inside the control panels, the detectors are for
alarm only.
The NMP1 auxiliary control room (relay room located below the main control room)
also has alarm-only ionization detectors inside relay-and-control panels.
However,
the NMP1 auxiliary control room also has an automatic cross-zoned total-flooding
halon system actuated by ionization detectors located in the overhead.
Cross-zoned
systems require a signal from at least one detector in two different zones to
automatically actuate the system.
The NMP1 auxiliary control room is separated
from the main control room by a fire door, and all penetrations
are sealed.
At
NMP2, the under-floor area of the control room has an automatic cross-zoned total-
flooding halon system.
The detection in this case is both ionization and thermal
detection.
One of each detector type must be actuated for halon suppression to
initiate. At NMP2, the under-floor area has access
panels that are covered by
carpet.
With the assistance
of operations personnel, the inspectors reviewed the fire
suppression
and detection systems in each control room, and identified no
discrepancies.
The inspectors discussed with the SSSs for both units and the fire
protection supervision to determine whether, in their opinion, actuation of the total-
flooding halon systems would require control room evacuation.
Although the
possibility existed for halon to seep into the control rooms, the leakage rate would
be slow and inhibited by the previously discussed
barriers.
The fire protection
supervisor stated that the potential for a distressful atmosphere would exist only if
the halon concentration became high or if it was breathed for, an unextended
period
of time.
In both cases,
halon system initiation should not affect control room
habitability to the extent that evacuation would be required.
However, if necessary,
both units have procedures
in place for control room evacuation.
Without a general
area automatic fire suppression
system specifically located in either control room,
30
the inspectors concluded that the concern associated with the Haddam Neck event
did not exist at Nine Mile Point.
Although there was no procedural guidance specifically directing operators to don
self-contained breathing apparatus
(SCBA), there could be situations when the use
of SCBAs by control room personnel would be necessary for short periods of time.
At both units, most control room personnel were trained and qualified to use
SCBAs; however, the SCBAs are primarily used by fire brigade members.
The
number of SCBAs and the number of spare bottles were specified in an Emergency
Plan Maintenance Procedure.
The equipment is surveilled monthly by fire protection
personnel to verify that the required number of usable SCBAs exist.
The inspectors
walked down the locations with fire protection personnel and reviewed the
applicable surveillance procedures to ensure that routine verifications were being
conducted.
If the control room staff needed to don SCBAs, there appeared to be a
sufficient quantity of SCBAs onsite.
The SCBAs, however, may need to be
obtained from locations other than directly outside the control room.
c.
Conclusions
The inspectors noted that the concern associated with the Haddam Neck automatic
fire suppression
system actuation did not exist at Nine Mile Point.
Plant personnel
appeared trained and equipped to combat a control room fire. Additionally,
procedures were in place should personnel evacuation of the control room be
required.
V. MANAGEMENTMEETINGS
X1
Exit Meeting Summary
At periodic intervals, and at the conclusion of the inspection period, meetings were
held with senior station management to discuss the scope and findings of this
inspection.
The exit meetings for specialist inspections contained within this report
were conducted upon completion of their onsite inspection:
Transportation and Radwaste Program
Radiological Protection Program
August 15, 1997
August 29, 1997
The final exit meeting occurred on October 17, 1997.
During this meeting, the
resident inspectors findings were presented.
NMPC did not dispute any of the
inspectors findings or conclusions.
Based on the NRC Region
I review of this report,
and discussions with NMPC representatives,
it was determined that this report does
not contain safeguards
or proprietary information.
ATTACHMENT1
PARTIALLIST OF PERSONS CONTACTED
Nia ara Mohawk Power Cor oration
R. Abbott
D. Barcomb
C. Beckham
D. Bosnic
J. Burton
H. Christensen
J. Conway
G. Correll
R, Dean
A. DeGracia
S. Doty
K. Dahlberg
G. Helker
P. Mazzafero
L. Pisano
R. Randall
P. Smalley
R. Smith
R. Tessier
C. Terry
K. Ward
C. Ware
D. Wolniak
Plant Manager, NMP1 (Acting)
Manager, NMP2 Radiation Protection
Manager, Quality Assurance
Manager, NMP2 Operations
Director, ISEG
Manager, Security
Vice President, Nuclear Engineering
Manager, NMP1 Chemistry
Manager, NMP2 Engineering
Manager, NMP1 Work Control
Manager, NMP1 Maintenance
Plant Manager, NMP2 (Acting)
Manager, NMP2 Work Control
Manager, NMP1 Technical Support
Manager, NMP2 Maintenance
Manager, NMP1 Engineering
Manager, NMP1 Radiation Protection
Manager, NMP1 Operations
Manager, Training
Vice President,
Nuclear Safety Assessment 5 Support
Manager, NMP2 Technical Support
Manager, NMP2 Chemistry
Manager, Licensing
INSPECTION PROCEDURES USED
IP 37551:
IP 61726:
IP 62707:
IP 71707:
IP 71750:
IP 83750:
IP 86750:
IP 90712:
IP 92700:
IP 92903:
IP 92904:
On-Site Engineering
Surveillance Observations
Maintenance Observation
Plant Operations
Plant Support
'Occupational Radiation Exposure Program
Solid Radwaste Management 5 Transportation of Radioactive Material
In-Office Review of Written Reports of Nonroutine Events at Power
Reactor Facilities
Onsite Followup of Written Reports of Nonroutine Events at Power
Reactor Facilities
Followup - Maintenance
Followup - Engineering
Followup - Plant Support
Prompt Onsite Response to Events at Operating Power Reactors
Implementation of Revised 49 CFR Parts 100-179 and 10 CFR Part 71
A-1
Attachment
1
ITENIS OPENED, CLOSED, AND UPDATED
OPENED
50-410/97-07-01
Failure to evaluate catch containment as a permanent
modification
50-410/97-07-03
50-410/97-07-04
50-220/97-07-05
50-220 5
50-410/97-07-06
50-220/97-07-07
50-220/97-07-08
IFI
50-220/97-07-09
50-220 5
50-410/97-07-10
50-220 8L
410/97-07-1
1
50-220 5
410/97-07-1 2
50-220/97-07-1 3
CLOSED
50-220 5
41 0/96-07-1 8
50-220/96-05-02
EEI
EEI
IFI
IFI
50-220/96-07-04
50-220/96-05-01
50-220/
EA-96-079-101 3
50-220/97-07-02
Missed TS SR on Channel
11 control room vent radiation
monitor
Missed TS SR on HCS instrumentation
Errors in calculation to support 1995 RB/TB blowout
panel modification
Inadequate
design control associated with smoke purge
system and CREVS interface
Failure to maintain PCP up-to-date
Radioactive shipment exceeded 49 CFR 173.441 limits in
occupied space of vehicle
Review action plan to ensure safe use of concentrates
tank 0'1, or removal of contents
Shipments of radioactive materials delivered to
unlicensed facilities
Shipment of wrong radioactive waste material
Failure to identify and correct conditions adverse to
quality associated with the PCPs
Failure to conduct audits of suppliers of NRC-certified
shipping casks
Failure to verify QA programs of Radwaste processing vendors
Poor material condition in several areas
Resolve inconsistencies
in reactor building and turbine
building blowout panel relief pressure values that are
Procedure change evaluation used to change the intent
of a procedure
Review of revised reactor and turbine building blowout
panel relief pressure calculations
Design control measure inadequate during calculation for
establishing the reactor and turbine building relief
pressure
A-2
Attachment
1
50-410/97-07-01
Failure to evaluate catch containment as a permanent
modification
50-220/97-07-05
50-410/97-06
50-41 0/97-07
LER
LER
50-220/97-07-04
Errors in calculation to support 1995 RB/TB blowout
panel modification
Inadequate design control associated with smoke purge
system and CREVS interface
Plant Shutdown due to Rising Unidentified Leakage
Failure to Calibrate Hydrogen Recombiner Instruments as
Required by Technical Specifications due to Procedure
Omission
50-220/97-07
UPDATED
none
LER
Potential Control Room Emergency Ventilation System
Operation Outside the Design Basis due to Inadequate
Evaluation
LIST OF ACRONYMS USED
CFR
CR
CRSPS
DER
EC
GL
GSO
IFI
IPAP
IR
IS.C
As Low As Reasonably Achievable
Code of Federal Regulations
Control Room
Control Rod Drive
Control Room Emergency Ventilation System
Control Room Smoke Purge System
Deviation/Event Report
Enforcement Action
Emergency Cooling
Escalated Enforcement Item
Exposure Evaluation Reports
Equipment Qualification
Generic Letter
General Supervisor of Operations
Hydrogen Recombiner System
High Pressure
Inspection and Enforcement
Inspector Follow Item
Integrated Performance Assessment
Process
Individual Plant Examination
Inspection Report
Instrumentation and Control
A-3
Attachment
1
kV
LCO
LDCR
LER
mR/hr
mRem/hr
NMP2
NRC
PM/ST
psf
Radwaste
SLS
SR
TS
tation Program
est
kiloVolt
Limiting Condition for Operation
Licensing Document Change Request
Licensee Event Report
Modular Accident Analysis Program
Motor-operated Valve
milliroentgen per hour
milliRem per hour
Non-Cited Violation
Niagara Mohawk Power Corporation
Nine Mile Point Unit 1
Nine Mile Point Unit 2
Nuclear Regulatory Commission
Office of Nuclear Reactor Regulation
National Voluntary Laboratory Accredi
Procedure Change Evaluation
Problem Identification
Preventive Maintenance/Surveillance
T
pounds per square foot
Quality Assurance
Radioactive Waste
Reactor Building
Radiologically Controlled Area
Reactor Core Isolation Cooling
Refueling Outage
Regulatory Guide
Radiation Protection
Radiation Work Permit
Small Article Monitor
Self-contained Breathing Apparatus
Surveillance Requirement
Source Range Monitor
Station Shift Supervisor
Turbine Building
Thermoluminescent Dosimeter
Technical Specification
Updated Final Safety Analysis Report
Violation
Work Order
A-4
0