ML17059B312

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Insp Repts 50-220/96-07 & 50-410/96-07 on 960602-0727. Violations Noted.Major Areas Inspected:Plant Operations, Maintenance,Engineering & Plant Support
ML17059B312
Person / Time
Site: Nine Mile Point  Constellation icon.png
Issue date: 10/08/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION I)
To:
Shared Package
ML17059B310 List:
References
50-220-96-07, 50-220-96-7, 50-410-96-07, 50-410-96-7, NUDOCS 9610150256
Download: ML17059B312 (68)


See also: IR 05000220/1996007

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

Docket/Report Nos.:

50-220/96-07

50-410/96-07

License Nos.:

DPR-63

NPF-69

Licensee:

Niagara Mohawk Power Corporation

P, O. Box 63

Lycoming, NY 13093

Facility:

Nine Mile Point, Units

1 and 2

'ocation:

Scriba, New York

Dates;

June 2, - July 27, 1996

Inspectors:

B. S. Norris, Senior Resident Inspector

T. A. Beltz, Resident Inspector

L. A. Peluso, Radiation Physicist

D. M. Silk, Senior Emergency Preparedness

Specialist

R. A. Skokowski, Resident Inspector

Approved by:

Lawrence T. Doerflein, Chief

Reactor Projects Branch

1

Division of Reactor Projects

96iOi50256 96i008

PDR

ADQCK 05000220

8

PDR

EXECUTIVE SUMMARY

Nine Mile Point Units 1 and 2

50-220/96-07

8E 50-410/96-07

June 2, - July 27, 1996

This integrated inspection report includes reviews of licensee operations,

engineering,

maintenance,

and plant support.

The report covers a 6-week period of resident inspection;

it also includes the results of inspections conducted

by regional inspectors

in the areas of

radiological environmental monitoring and meteorological monitoring, and emergency

preparedness.

The report also contains

a review of the NRC Integrated Performance

Assessment

Process

(IPAP) team inspection report.

During the IPAP report review, the

inspectors identified violations, unresolved

items, and inspection followup items, a

summary of which is provided in Attachment A to this report.

PLANT OPERATIONS

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The Unit 1 operators acted appropriately and completed actions in accordance

with

procedures

during the June 6, 1996, feedwater heater level transient.

The root cause

in the deviation/event report (DER) was accurate,

and appropriately supported.

NMPC's

review to identify potential damage was good, and included structural, fuel, and core

shroud analyses.

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During the review of an October 1994 Unit 2 LER, the inspectors determined that there

were several missed opportunities for the shift management to identify the correct

technical specification (TS) action statement when authorizing concurrent work on

multiple hydraulic control unit accumulators.

In addition, the work control/planning

organization could have aided the operations staff by including the potential plant

impact as part of the work package.

Nonetheless,

once identified, the shift crew took

prompt action to ensure the plant was in compliance with the TS. This was identified

as a non-cited violation.

MAINTENANCE

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In general, maintenance

and surveillance work was conducted

professionally, with the

necessary

procedures

at the work site, and with the appropriate focus on safety.

As

necessary,

the proper radiation protection work practices were implemented.

~

The Unit

1 operations

personnel

perform'ed well on all aspects of a routine emergency

diesel generator surveillance, accomplished the evolution without incident, and

appeared to understand

the scope of the surveillance.

Communications between the

operators

in the turbine building and the control room were adequate.

~

As a result of corrective actions associated

with earlier LERs, NMPC discovered

additional surveillances that had not been performed as required.

Unit

1 failed to

calibrate one of the instruments for the containment leakage detection system during

the last two refueling outages;

and Unit 2 did not test several valves in the reactor core

0

Executive Summary (cont.)

isolation cooling system prior to reactor system pressure

exceeding

150 psig. The root

causes were different, and each was identified as a non-cited violation.

~

Unit 2 maintenance

technicians performed receipt inspections of new fuel appropriately

and in accordance

with the procedure.

Storage and handling activities associated

with

the shipping crates and the fuel assemblies

on the refuel floor were verified to be in

accordance

with licensing conditions.

ENGINEERING

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The check valves for the service water system to the unit cooler in the Unit 2 high

pressure

core spray (HPCS) switchgear room failed the forward and reverse flow tests

during a routine surveillance, resulting in the HPCS system being inoperable longer than

expected.

The inspectors noted that the licensee's

past corrective actions to address

this issue have not been fully effective.

Additional management

attention to this issue

is warranted.

~

A Unit 1 LER identified that the TS limitfor the power to flow ratio was exceeded

for

about 5.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> due to the reactor recirculation flow instruments being recalibrated

using a new methodology.

The new method resulted in a indicated flow reading higher

than actual flow if the transmitter was isolated.

After the last refueling outage, the unit

restarted with one recirculation loop isolated.

The cause of the event was an

inadequate

understanding

of the new method and the potential impact on plant

operations.

This was identified as a non-cited violation.

PLANT SUPPORT

~

NMPC continued to implement an effective overall radiological environmental

monitoring program and meteorological monitoring program including management

controls, quality assurance

audits, and quality assurance

of analytical measurements.

The offsite dose calculation manual was properly implemented.

Audits were effective

in assessing

program strengths

and weaknesses.

~

A review of revisions to the emergency

plan and implementing procedures

determined

that the revisions did not reduce the effectiveness of the emergency

plan and were

acceptable.

TABLE OF CONTENTS

page

EXECUTIVE SUMMARY

TABLE OF CONTENTS

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IV

SUMMARY OF ACTIVITIES

1

Niagara Mohawk Power Corporation (NMPC) Activities

Nuclear Regulatory Commission

(NRC) Staff Activities ~......

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1

I. OPERATIONS

2

01

Conduct of Operations...

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2

01.1

General Comments

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02

Operational Status of Facilities and Equipment

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02.1

Unit 1 Loss of One String of Feedwater Heating

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2

07

Quality Assurance

in Operations ........ ~..........., ~......

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07.1

Review of INPO Evaluation .........

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3

08

Miscellaneous Operations

Issues

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08.1

(Closed) LER 50-410/95-12 and LER 50-410/95-12, Supplement

1:

Automatic Actuation of Standby Gas Treatment System Because of

Inadequate

Corrective Action for Snow Plugging of Filters..... ~.....

4

08.2

(Closed) LER 50-220/96-04:

Reactor Scram Caused by Turbine Trip Due

to Feedwater Oscillations ........... ~.........

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08.3

(Closed) LER 50-410/94-06:

Technical Specification Violation Resulting

from a Missed Action Statement

Caused by Inadequate

Work Practices

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08.4

(Closed) Unit 1 Special Report:

¹11 Suppression

Chamber Water Level

Monitoring System Inoperable .................... ~,...,,

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II. MAINTENANCE

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M1

Conduct of Maintenance

M1.1

General Comments

M1.2

Unit 1 EDGs and Power Board 102/103 Operability Testing.....

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M2

Maintenance

and Material Condition of Facilities and Equipment ..

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M2.1

Receipt Inspection of Unit 2 New Fuel (60705)

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M8

Miscellaneous Maintenance

Issues .............,.,

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M8.1

(Closed) LER 50-220/95-03, Supplement

1: Technical Specification

Surveillance Tests not Performed at the Required Frequency

Because of

Cognitive Error

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M8.2

(Closed)

LER 50-410/96-05:

Surveillance Requirement Not Performed Per

Technical Specifications Due to Inadequate Work Practices..........

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M8.3

(Closed) LER 50-410/96-07:

Technical Specification Violation Due to

Inadequate

Work Organization/Planning .....

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III. ENGINEERING .................

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E2 Engineering Support of Facilities and Equipment......................

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E2.1

Unit 2 HPCS Inoperable due to Failed Service Water Surveillance.....

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IV

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Table of Contents (cont'd)

E8 Miscellaneous

Engineering

Issues

E8.1

(Closed) LER 50-220/96-03:

Power to Flow Technical Specification

Violation due to Ineffective Change Management

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IV. PLANT SUPPORT...

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R1 Radiological Protection and Chemistry (RP&.C) Controls ..

R1.1

Implementation of the Radiological Environmental Monitoring

(84750)

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R1.2

Meteorological Monitoring Program (84750)

R6 RP&C Organization and Administration

R6.1

Organization Changes

and Responsibilities (84570)

R6,2

Annual Environmental Operating Report (84570)

R7 Quality Assurance

in RPSC Activities

R7.1

Quality Assurance Audit Reports (84750)

R7.2

Quality Assurance of Analytical Measurements

(84750)

P3 EP Procedures

and Documentation

P3.1

In-Office Review of Changes to the E-Plan (82701)

V. Management Meetings........

X1

Exit Meeting Summary....

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X3

Management

Meeting Summary

X3.1

Regional Drop-In Visit by Executive Vice President

Program

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PARTIALLIST OF PERSONS CONTACTED .... ~.... ~.......

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INSPECTION PROCEDURES USED....

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ITEMS OPENED, CLOSED, AND UPDATED....

LIST OF ACRONYMS USED

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ATTACHMENT

ATTACHMENTA -

RESULTS OF THE REVIEW OF NRC IPAP IR 50-220/96-201

AND

50-410/96-201: LIST OF VIOLATIONS, UNRESOLVED ITEMS, AND

INSPECTOR FOLLOW ITEMS

0

REPORT DETAILS

Nine Mile Point Units 1 and 2

50-220/96-07

8( 50-410/96-07

June 2- July 27, 1996

SUMMARYOF ACTIVITIES

Niagara Mohawk Power Corporation (NMPC) Activities

Unit 1

Nine Mile Point Unit 1 (Unit 1) started the inspection period at full power.

On June 6,

power was reduced to 80% to repair the ¹12 feedwater heater string; power was returned

to 100% on June 11.

On July 19, power was reduced to 45% to allow cleaning of the

north condenser water box.

On July 21, the ¹13 shaft driven feedwater pump would not

engage,

limiting reactor power to 45% to the end of the period.

Unit 2

Unit 2 maintained essentially full power throughout the period.

On June 15, power was

reduced to 50% to allow for a shift of feedwater pumps, power was returned to 100% on

June 16.

On July 19, power was reduced to 78% for a control rod pattern adjustment,

full power was restored on June 20.

Nuclear Regulatory Commission (NRC) Staff Activities

lns ection Activities

The NRC resident inspectors conducted

inspection activities during normal, backshift, and

weekend hours.

There was one specialist inspection conducted

during this period in the

area of radiological environmental monitoring and meteorological monitoring; also, an in-

office review was performed regarding changes to the emergency

plan and the associated

procedures.

The results of the inspection and the review are contained

in this report.

During this period, the resident inspectors reviewed the report of the NRC Integrated

Performance Assessment

Process

(IPAP) team inspection conducted from March 4 through

22, 1996 (NRC Inspection Report 50-220/96-201

and 50-410/96-201).

By charter, the

NRR IPAP team inspections do not evaluate their findings with respect to enforcement;

therefore, the inspectors reviewed the IPAP report to identify violations, unresolved items,

and inspection follow items.

Some items identified by the IPAP team had been previously

identified or addressed

in earlier NRC inspection reports.

A summary of the issues

identified is provided in Attachment A to this report.

U dated Final Safet

Anal sis Re ort

UFSAR Reviews

A recent discovery of a licensee operating their facility in a manner contrary to the UFSAR

description highlighted the need for additional verification that licensees were complying

with UFSAR commitments.

While performing the inspections discussed

in this report, the

0

inspectors reviewed the applicable portions of the UFSAR related to the areas inspected.

The inspectors verified that the UFSAR wording was consistent with the observed

plant

practices, procedures

and/or parameters.

I. OPERATIONS

01

Conduct of Operations

(71707)'1.1

General Comments

Using Inspection Procedure 71707, the inspectors conducted frequent reviews of

ongoing plant operations.

In general, operations were conducted

professionally and

with the proper focus on safety; specific events and noteworthy observations

are

detailed in the sections below.

02

Operational Status of Facilities and Equipment (71707)

02.1

Unit 1 Loss of One Strin

of Feedwater

Heatin

a.

Ins ection Sco

e

The inspector reviewed the details associated

with the June 6, 1996, feedwater

heater level control transient at Unit 1. The review included the applicable portions

of the chief station operator (CSO) and station shift supervisor (SSS) logs for the

event, and a discussion of the event with membeis of the operating crew and Unit

1 plant management.

The inspectors walked down areas of the plant effected by

the transient.

The inspectors also reviewed the deviation/event report (DER) written

to address the event, and the applicable portions of the Unit

1 UFSAR and Technical

Specifications (TSs).

b.

Observations

Findin s

At 4:02 a.m. on June 6, 1996, while at 100%, Unit 1 experienced

a level transient

in feedwater heating string ¹12.

Control room operators reduced power to 98.5%,

and attempted to restore water level for feedwater heaters ¹123 and ¹122 (third

stage heater and second stage heater, respectively, in string 12).

Operators noted

that the ¹122 feedwater heater piping had moved, due apparently to water flashing

to steam within the system.

At 4:40 a.m., operators reduced power below 80%

and isolated feedwater heater string ¹12.

Operators acted appropriately and

completed necessary

actions in accordance

with procedures.

'opical headings such as 01, M8, etc., are used in accordance withthe NRC standardized reactor inspection report outline.

Individual reports are not expected to address

all outline topics.

The NRC Inspection manual procedure or temporary

Instruction that was used as Inspection guidance Is listed for each applicable report section.

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To assess

the significance of operating with a loss of a feedwater heater string, the

inspectors reviewed the applicable portions of the Unit 1 UFSAR and TS. At Unit 1,

the feedwater heaters

are part of the flow path for the high pressure coolant

injection (HPCI) system.

The UFSAR states that HPCI is not an engineering

safeguards

system nor is it considered

in any loss of coolant accidents

analyses.

However, according to the TS, HPCI ensures

adequate

core cooling in the event of

a small reactor coolant line break.

The inspectors verified that only one of the three

feedwater heater strings are required for HPCI operability.

Later, on June 6, the inspectors, with Unit

1 personnel,

walked down portions of

the ¹12 feedwater heater string, including the heaters

and the associated

feed and

steam piping, to assess

the damage.

A piping support for extraction steam to

feedwater heater ¹122 was found disengaged

from the concrete wall, with some

damage to the concrete.

Three other pipe supports for feedwater heater ¹122 were

found bent.

Other components

associated

with the feedwater heater were also

found damaged.

NMPC determined the root cause to be a failure of the level control valve for

feedwater heater ¹122.

To evaluate the effect of the transient, NMPC performed

the following: an analysis to verify that system integrity was not structurally

comprised;

an analysis to verify no adverse affect to the reactor or fuel; and an

assessment

to verify no affect on the core shroud.

The results of the evaluations,

as well as the root cause analysis of the event, were described

in DER 1-96-1389.

The Station Operations Review Committee (SORC) reviewed and approved the

proposed

repairs and related evaluations associated

with the event.

Repairs to the

system were completed on June 10; feedwater heater string ¹12 was returned to

service and the plant was returned to full power on June 11.

The inspectors considered the root cause described

in the DER to be accurate,

and

appropriately supported

by the physical evidence of the valve condition and

computer data for the feedwater heater string ¹12 drain cooler flows.

C.

Conclusion

The inspectors found that the Unit

1 operators acted appropriately and completed

actions in accordance

with procedures

during the June 6, 1996, feedwater heater

level transient.

The root cause described

in the DER was accurate,

and

appropriately supported with physical evidence and computer data.

NMPC's review

to determine the potential damaged

cause by the transient was good, as evidenced

by the completion of the structural, fuel and core shroud analysis.

07

Quality Assurance in Operations (71707)

07.1

Review of INPO Evaluation

The inspectors reviewed the report from the Institute of Nuclear Power Operations

(INPO) evaluation conducted from January 29 through February 9, 1996.

The

evaluation examined the overall operation of the Nine Mile Point site, and was

0

performed by peer evaluators from other nuclear facilities. The report identified no

issues that the NRC was not already aware of, and no additional followup by the

NRC is warranted.

08

Miscellaneous Operations Issues (90712, 90713, 92700)

08.1

Closed

LER 50-410 95-12 and LER 50-410 95-12

Su

lement 1: Automatic

Actuation of Standb

Gas Treatment

S stem Because of Inade

uate Corrective

Action for Snow Plu

in

of Filters

On December 11, 1995, with Unit 2 operating at 100% power, the standby gas

treatment system (GTS) automatically initiated and the normal reactor building

ventilation systems isolated.

Heavy snowfall and gusty winds caused snow to

accumulate

on the inlet filters for the normal reactor building ventilation.

The

purpose of the inlet filters was to remove dust, dirt, and insects, to protect the

ventilation cooling coils.

During the winter months, the cooling coils are not in

service and the system could be operated without the filters.

The shift operators were aware of the decreasing

air flow and dispatched

personnel

to remove the filters from service.

However, before the filters could be removed

from service, the reactor building ventilation isolated with a concurrent automatic

initiation of GTS, due to a low exhaust air flow. Subsequently,

the filters were

removed, and ventilation was returned to normal.

Licensee Event Report (LER) 50-410/95-12 was first reviewed in NRC Inspection

Report (IR) 50-410/96-01; it identified the root cause as being inadequate

corrective

actions to previously identified problems.

Particularly, NMPC noted that similar

ventilation degradations

had been experienced

in the 1980's, caused

by snow

plugging of the filters. The LER was not closed during the initial review because the

listed corrective actions only addressed

preventing the inlet filters from again

clogging with snow, not the root cause.

Therefore, as discussed

in IR 50-410/96-

01, the licensee agreed to submit a supplement to the LER that described

completely the corrective actions to address

all root causes.

To address the root cause of inadequate

corrective actions,

LER 50-410/95-12,

Supplement

1, was issued to provide additional information regarding enhancements

that had already been made to the NMPC problem resolution process.

The process

for problem resolution was contained

in procedure

NIP-ECA-01, "Deviation Event

Reports," and included increased oversight of problem evaluations,

assignment

of

trend codes and more stringent requirements for root cause evaluations.

The

inspectors considered the corrective actions appropriate to address the root cause.

08.2

Closed

LER 50-220 96-04:

Reactor Scram Caused

b

Turbine Tri

Due to

Feedwater Oscillations

On May 20, 1996, Unit 1 experienced

a turbine trip and reactor scram from 100%

power.

The turbine trip was due to a high reactor vessel water level, caused by a

failure of the ¹13 feedwater flow control valve.

0

The description of the event in the LER, including the root cause analysis and

corrective actions, was consistent with the inspectors'eview

of the event, as

documented

in NRC IR 50-220/96-06.

08.3

Closed

LER 50-410 94-06: Technical S ecification Violation Resultin

from a

Missed Action Statement

Caused

b

Inade

uate Work Practices

a.

Ins ection Sco

e

This LER describes

an event which happened

in October 1994, but the LER had not

been reviewed previously due to an administrative oversight.

The inspectors

reviewed the details of the event and the associated

LER, the applicable portions of

the CSOs and SSS logs for the event, and discussed

the event with Unit 2 plant

management.

The inspectors

also reviewed the applicable portions of the Unit 2

TSs.

b.

Observations

Findin s

During the work control planning process,

Unit 2 scheduled two control rod drive

(CRD) hydraulic control unit (HCU) accumulators to be worked the same day.

The

affected departments

(maintenance,

work control/planning,

and operations)

had

agreed to work the HCUs sequentially,

and had noted this in an attachment to the

weekly work schedule.

However, the agreed upon schedule was not included in the

plant impact section of the individual work packages.

Subsequently,

on October

24, 1994, with Unit 2 operating at 90% power, shift management

allowed two

HCU accumulators to be made-inoperable

without'implementing the required TS

action statements.

Specifically, per TS 3.1.3.5, when an accumulator is inoperable, the associated

control rod is also inoperable.

Ifthe control rod is inoperable for reasons other than

being immovable due to friction or binding, then per TS 3.1.3.1.b, two options

exist:

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insert the control rod and disarm the associated

directional control valves; or

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if the control rod is withdrawn, verify it is separated

from all other inoperable

control rods, and insert the control rod at least one notch using normal drive

water pressure.

TS 3.1.3.5, action statement a.2.a, states that with more than one accumulator

inoperable,

and the associated

control rods withdrawn, immediately verify at least

one CRD pump operating by inserting at least one control rod at least one notch.

If

a pump is not running, start a CRD pump within 20 minutes and insert at least one

control rod one notch, or place the reactor mode switch in the shutdown position.

When the station shift supervisor (SSS) reviewed and approved the first HCU work

package, the SSS and the assistant

SSS (ASSS) recognized that the control rod was

required to be declared inoperable.

When the second

HCU work package was

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reviewed and approved, the SSS knew that a withdrawn control rod needed to be

inserted at least one notch to verify CRD pump operability, but failed to inform the

ASSS of the additional requirement due to the second control rod accumulator being

inoperable at the same time. The chief shift operator (CSO) questioned the

appropriateness

of having multiple accumulators out of service; the ASSS reviewed,

but misinterpreted, the TSs.

The second control rod was declared inoperable ten

minutes after the first. The ASSS again reviewed the TSs while logging the above

into the SSS log. At this point, he recognized that they had not complied with the

requirement for inserting a control rod one notch.

Twenty-five minutes after the

second control rod was inoperable,

a different control rod was inserted one notch;

meeting TS requirements.

The root cause was an inadequate

review by the SSS and ASSS; contributing

causes were poor verbal communications

between the SSS and ASSS, and poor

work coordination that allowed both HCUs to be worked at the same time.

Corrective actions included counseling of all SSSs and ASSSs, emphasis

on TS

implementation during licensed operator requalification training, and enhancements

to the work control process.

The inspectors verified that the LER description of the event was consisted with the

sequence

of events as documented

in the control room logs; the inspectors

also

discussed

the LER with Unit 2 operations management.

The failure to take the

required actions as detailed in the limiting condition of operation for multiple

inoperable

CRD HCU accumulators,

as described

above,

is a violation of the Unit 2

Technical Specifications, Section 3.1.3.5.a.2.a.

However, because this licensee

identified event occurred almost two years ago, and the corrective actions appear to

have prevented recurrence, this violation is being treated as a Non-Cited Violation,

consistent with Section VII.B.1 of the NRC Enforcement Policy,

C.

Conclusion

The inspectors

noted that there were several chances for the shift management to

identify the correct TS action statement;

during the initial review of the work

packages

by the SSS and ASSS, and when questioned

by the CSO.

In addition, the

work control/planning organization could have aided the operators by including the

potential plant impact as part of the work package.

Nonetheless,

once identified,

the shift crew took prompt action to ensure the plant was in compliance with the

TS.

In addition, NMPC management

took adequate

corrective actions to prevent

recurrence.

OSA

Closed

Unit 1 S ecial Re ort: ¹11 Su

ression Chamber Water Level Monitorin

S stem lno erable

On July 11, 1996, with Unit 1 at 100% power, NMPC removed the ¹11

suppression

chamber water level (SCWL) monitoring system from service for

troubleshooting

of an erroneous

high level alarm.

Technicians recalibrated the

transmitter and adjusted the alarm setpoint, and returned the system to operable the

same day.

The redundant train of SCWL remained operable.

NMPC submitted

a

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special report to the NRC within 14 days, as required by the Unit 1 Technical

Specificationl (TS) 3.6.11-1, action statement 4.a;

The inspectors reviewed the

special report, and confirmed that all required information was contained

in the

report.

II.

MAINTENANCE'1

Conduct of Maintenance

M1.1

General Comments

Using Inspection Procedures

61726 and 62703, the inspectors observed

plant

maintenance

activities and the performance of various surveillance tests.

In

general, maintenance

and surveillance activities were conducted

professionally, with

the work package

and necessary

procedures

at the work site and in use, and with

the appropriate focus on safety.

As necessary,

the proper radiation protection work

practices were implemented.

Specific activities and noteworthy observations

are

detailed in the sections below.

The inspectors observed

all or portions of the

following maintenance

and surveillance activities:

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N2-ISP-NMS-W@001

Unit 2 - APRM Channel Functi

M1.2

Unit

1 EDGs and Power Board 102 103 0 erabilit

Testin

~

N1-ST-M4

EDGs/PB 102 and 103 Operability Test

~

N1-ISP-083-001

Drywell Liquid Waste Flow Meters

~

N2-MMP-FHP-099

Receiving, Inspecting, and Storage of New Fuel

'onal Test

a.

Ins ection Sco

e

On July 22, 1996, the inspectors observed operator performance of surveillance

procedure

N1-ST-M4, Revision. 24, "EDGs/PB [Emergency Diesel Generators/Power

Board] 102 and 103 Operability Test."

Specifically, Section 8.3, "Diesel Generator

103 One Hour Performance

Run," of the reference procedure was observed.

b.

Observations

and Findin s

The inspectors observed operations staff performing the surveillance locally in the

Unit 1 Turbine Building. The operators performed the following evolutions:

/

~

hand-jacking of EDG 103 and integrity check of 20 cylinder test valves

~

EDG operability checks prior to load run

~

remote starting of EDG 103 and verification that the EDG obtained proper speed

and voltage in allowable time

Surveillance activities are included under "IVlalntenance." For exemple. a section involving surveillance observations might

be Included as a separate sub.topic under M1, " Conduct of Maintenance."

0

~

load run

Communications

between the operators

in the turbine building and the control room

were adequate.

The inspectors

also observed the markup of the EDG for

performance of the hand-jacking evolution, and noted conformance with plant policy

concerning independent

verification of the markup and subsequent

valve

restoration.

No concerns were identified.

Starting of the EDG and subsequent

load

run were monitored by the inspectors, with no identified concerns.

c.

Conclusions

The inspectors noted that operations

personnel performed all aspects

of the EDG

surveillance test well. The inspectors determined that the staff appeared

to'nderstand

the scope of the surveillance and accomplished the evolution without

incident.

M2

Maintenance and Material Condition of Facilities and Equipment

M2.1

Recei t Ins ection of Unit 2 New Fuel 60705

The inspectors observed the inspection of new fuel for the upcoming refueling

outage at Unit 2. Technicians completed the inspections

in accordance

with

procedure

N2-MMP-FHP-099, Revision 2, "Receiving, Inspection, and Storage of

New Fuel." The inspectors verified that the receipt/inspection

activities complied

with the Unit 2 licensing conditions associated

with fuel storage and handling.

The

inspectors concluded that the new fuel handling activities were appropriately

completed.

MS

Miscellaneous Maintenance Issues

M8.1

Closed

LER 50-220 95-03

Su

lement 1: Technical S ecification Surveillance

Tests not Performed at the Re uired Fre uenc

Because of Co nitive Error

On June 13, 1996, as a result of corrective actions associated

with LER 95-03,

NMPC discovered

an additional instrument and control (ISC) surveillance procedure

had not been performed within the frequency required by TSs.

Specifically, TS

surveillance requirement

(TSSR) 4.2.5.b.(1) required performance of an instrument

calibration on each containment leakage detection system once each refueling

outage.

The TS bases discussed

three subsystems

for containment leak detection:

rate of rise leak detection; timer leak detection; and integrated flow rate.

These

three leak detection systems

are independent

and utilize separate

surveillance

procedures for performing functional testing and instrument calibration.

The rate of rise and timer leak detection system instrument functional tests and

calibrations were performed during refueling outages

12 and 13 (RFO-12 and RFO-

13).

The integrated flow rate instrument functional test and calibration was

accomplished

by surveillance procedure N1-ISP-083-001, "Drywell Liquid Waste

Flow Meters".

NMPC identified this surveillance had been completed satisfactorily

0

during quarterly surveillance prior to, and subsequent

to, RFO-12 and RFO-13.

However, the refueling outage TSSR was not performed during either RFO-12 or

RFO-13.

Since this was another example of a surveillance test not being performed

during the refueling outage as required, NMPC issued Supplement

1 to LER 95-03

on July 13, 1996.

LER 95-03 was originally discussed

and closed as part of NRC IR 50-220/95-16.

The inspectors reviewed the LER Supplement

and determined that it satisfactorily

described the event, the root cause evaluation, and corrective actions to prevent

similar occurrences

in the future.

The failure to perform the calibration at the

required periodicity is a violation of TSSR 4.2.5.b(1); based on the corrective

actions and low safety consequence,

this licensee identified violation is being

treated as a Non-Cited Violation, consistent with Section VII.B.1 of the NRC

Enforcement Policy.

M8.2

Closed

LER 50-410 96-05:

Surveillance

Re uirement Not Performed Per Technical

S ecifications Due to Inade

uate Work Practices

On April~15, 1996, while Unit 2 was operating at approximately 100% power,

control room operators discovered that during the performance of Division 3 service

water operability testing, the Division 3 EDG had not been declared inoperable

as

required by TS. This resulted in the failure to perform TS SR 4.8.1

~ 1, verification of

breaker alignment and power availability, within one hour as required by TS 3.8.1.1.

The failure to declare the Division 3 EDG inoperable was identified by the control

room operators approximately three hours after the beginning of the service water

testing, when the ASSS was informed that a check valve failed its reverse flow

test. At this time, the ASSS and SSS recognized that the EDG should have been

declared inoperable at approximately 12:45 p.m. when the surveillance testing

began.

The SR was satisfactorily completed at approximately 3:45 p.m. ~

The root cause of the event, as described

in the LER, was inadequate

work practice

by the ASSS.

During the ASSS's review of the service water surveillance test, he

identified that the EDG would become inoperable.

However, instead of consulting

the TS to determine the applicable action statement requirements,

he continued his

review of the surveillance for other plant impacts.

This resulted in the failure of the

ASSS to declare the EDG inoperable and subsequent

failure to met the TS action

statement requirement.

NMPC identified two contributing factors:

the operator

performing the surveillance did not understand

management's

expectation

regarding

the procedure step to discuss the plant impact with the SSS and CSO, therefore the

discussion was not in the depth intended.

Secondly, the surveillance procedure

did

not direct the performance of the TS required actions for this short duration LCO.

The corrective actions for this event, as described

in the LER, included counseling

the SSS and ASSS regarding the need to fully read, comprehend

and initiate

compensatory

action for all TS requirements

prior to allowing work to commence.

Also, clarification was provided to all operators with respect to the requirement to

discuss the plant impact statement during the work approval process.

Additionally,

10

NMPC'planned to evaluate station procedures

to determine which should include

steps for completing applicable TS required actions.

The inspectors reviewed the LER and determined that it satisfactorily described the

event, the root cause,

and corrective actions to prevent similar occurrences

in the

future.

Based on the adequate

corrective actions and low safety consequence

this

licensee identified violation is being treated as a Non-Cited Violation, consistent

with Section VII.B.1 of the NRC Enforcement Policy.

Closed

LER 50-410 96-07:

Technical S ecification Violation Due to lnade

uate

Work Or anization Plannin

Unit 2 identified additional historical violations of TS surveillance requirement 4.0.4

as a result of the corrective actions associated

with Unit 2 LER 96-02.

Specifically,

on May 20, 1996, NMPC identified that several valves in the reactor core isolation

cooling (RCIC) system were not tested prior to reactor system pressure

exceeding

150 psig.

TS 3.7.4 requires the RCIC system be operable when reactor steam

pressure

is greater than 150 psig; TS surveillance 4.7.4.b requires that the RCIC

pump develop

a minimum flow of 600 gpm when steam pressure

at the turbine is

935-1035 psig.

Because steam pressure

is required to test the RCIC pump, TS 4.0.5 [inservice inspection (ISI) and inservice testing (IST)] allows the test to be

performed up to 12 hours1.388889e-4 days <br />0.00333 hours <br />1.984127e-5 weeks <br />4.566e-6 months <br /> after adequate

steam pressure

is available.

The associated

surveillance test procedure (N2-OSP-ICS-05002,

"RCIC Pump and

Valve Operability Test and System Integrity Test and ASME XI Functional Test" )

also tests several RCIC system valves on the water (discharge)

side of the pump.

The pump must be running to test the valves; accordingly, the valves also cannot

be tested until steam pressure

is adequate.

However, NMPC identified that three of

the valves in the procedure do not need the RCIC system to be in operation.

Therefore, because

TS 3.7A requires the valves to be operable, the surveillance

test for those three valves must be completed prior to exceeding

150 psig.

NMPC

determined that these valves had not been tested within the required time frame of

three occasions

(April 1, 1989, January 24, 1991, June 17, 1992).

NMPC

determined the cause to be inadequate

work organization and planning, because

several surveillance requirements were incorporated into one procedure without

accounting for different scheduling criteria.

No immediate corrective actions were required.

The actions planned to prevent

recurrence

included revising the IST program plan to identify which RCIC valves can

be delayed for testing, and revising the RCIC surveillance procedure to identify

which valves must be tested prior to exceeding

150 psig.

The inspectors noted that this was identified as a result of a previous event, which

heightened

the awareness

to the requirement of TS 4.0.4; and to ensuring that

required surveillance are performed at the proper frequency.

Based on adequate

planned corrective actions and low safety consequence

this licensee identified

violation is being treated as a Non-Cited Violation, consistent with Section VII.B.1

of the NRC Enforcement Policy.

11

III. ENGINEERING

E2

Engineering Support of Facilities and Equipment

E2.1

Unit 2 HPCS Ino erable due to Failed Service Water Surveillance

a 0

Ins ection Sco

e

On July 8, 1996, check valves in the service water system to the high pressure

core spray (HPCS) switchgear unit cooler failed to meet the forward and reverse

flow as required by the surveillance test.

The inspectors reviewed the operating

logs, the associated

work packages,

related DERs and the engineering'valuation.

The inspectors

also reviewed the surveillance history of the valves, and had

discussions

regarding recurring surveillance failures with the system engineer and

Unit 2 plant management.

b.

Observations

Findin s

On July 8, 1996, Unit 2 personnel conducted

a surveillance test

(N2-OSP-SWP-0005,

"Division 3 Service Water Operability. Test" ) of the service

water system associated

with the HPCS system.

During performance of this

procedure, the check valve to the HPCS unit cooler failed to meet the acceptance

criteria for both forward and reverse flow. After several attempts to clean the

system and repair the valves, the reverse flow portion of the N2-OSP-SWP-Q005

surveillance test was completed satisfactorily.

Engineering was able to provide a

lower minimum acceptance

criteria for forward flow, and the surveillance test was

completed satisfactorily on July 12.

The inspectors review of the operating logs, the associated

work packages,

and the

engineering evaluation identified no problems.

However, the inspectors noted that

each time the quarterly surveillance test has been performed since the beginning of

the year, the same valves have caused the HPCS system to become inoperable

(January 23-25, April 16-19, and July 8-12).

Furthermore,

in IR 50-410/95-24, the

inspectors documented

failures of the same surveillance and that Simple Design

Change SC2-0034-94 was ineffective in that it required additional design changes

to corrected the recurring surveillance test failures.

In Spring 1995, SC2-0034-94

was installed, which replaced the original piston check valves with nozzle check

valves. During the evaluation of a failed surveillance completed on October 30,

1995, NMPC recognized that the clearance between the plug and the seat of the

new valves was too narrow for the maximum expected

mussel size (1/8 inch) to

pass through.

In February 1996, NMPC changed the internals of these valves to

provide a larger clearance.

However, this February change was also ineffective as

evidenced by the continuing surveillance test failures.

When HPCS was inoperable in April, Unit 2 management

informed the resident

inspectors that one option being considered was removal of the unit cooler check

valves.

The inspectors consider the delay in finding a final resolution for the

12

problem with the unit cooler check valves is causing the HPCS system to be

unnecessarily

inoperable.

When discussing this concern with the Unit 2 Plant

Manager, it was brought to the inspector's attention that a DER (DER 2-96-1598)

had been initiated on July 8 to document both the current failed surveillance and the

repetitive failures.

The inspector reviewed the DER and the attached

engineering operability

determination checklist.

The DER listed the apparent cause

as due to fouling and

corrosion of small bore piping, some of it due to the treatment for clams in the

service water system (Clam-Trol) ~ A contributing cause was the failure to revise the

inservice testing (IST) acceptance

criteria after the earlier failures.

Each time the

valves failed the surveillance,

an operability determination was completed to accept

the values for that specific surveillance, but the IST database

was never changed.

The corrective actions include the issuance of a design document change

(DDC) to

change the IST database

and the associated

surveillance procedure.

In addition,

engineering will process the safety evaluation to support removal of the check

valves from the system; the valves are scheduled to be removed by the end of the

year.

C.

Conclusion

The inspectors considered the delay in finding a final resolution for the problems

associated

with the unit cooler check valves was causing the HPCS system to be

unnecessarily

inoperable.

Additional management

attention is warranted to ensure

future corrective actions are effective.

E8

Miscellaneous Engineering Issues

E8.1

Closed

LER 50-220 96-03:

Power to Flow Technical S ecification Violation.due to

Ineffective Chan

e Mana ement

The inspectors reviewed the LER, which discussed

the identification, by Unit 1

management

on May 9, 1996, that the TS limitfor power to flow ratio (PFR) had

been exceeded

for about 5.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> on April 8-9, 1995.

During the last Unit 1

refueling outage,

Spring 1995, the recirculation flow instruments were recalibrated

using a new methodology because

of lessons

learned from the reactor recirculation

pump runback on February 1, 1995.

The new method incorporated parameters that

resulted in an indicated reactor coolant flow reading higher than actual flow if the

transmitter was isolated or equalized.

After the outage, the plant restarted using

only 4 of the 5 recirculation loops; the idle loop transmitter was isolated, per the

operating procedure.

The combination of the new calibration method, and the

isolated transmitter resulted in an incorrect indicated flow in the idle loop of two

million pounds mass per hour (2E6 Ibm/hr) instead of 0 Ibm/hr.

About one week after startup, the system engineer identified the problem and the

transmitter was unisolated and placed in service, providing an accurate indication of

loop flow. Initial evaluation by NMPC, ba'sed on a review by engineering

and the

vendor, determined that the error did not cause the total recirculation flow to be

13

exceeded,

but the affect on the PFR correction factor was uncertain.

On May 7,

1996, after additional information became available,

a re-evaluation was performed;

this evaluation indicated that the PFR had been exceeded.

NMPC performed an

analysis of the event and verified that no fuel limits had been exceeded,

and

therefore, no cladding or fuel damage occurred.

The cause of the event was an

inadequate

review and understanding

of the new calibration methodology and the

potential impact on plant operations.

The inspectors reviewed the LER and determined that it satisfactorily described the

event, the root cause,

and corrective actions.

Completed and planned corrective

actions appear adequate to prevent similar occurrences

in the future.

However,

exceeding the PFR is a violation of TS 3.1.7.d, "Power Flow Relationship During

Operation".

This licensee identified violation is being treated as a Non-Cited

Violation, consistent with Section VII.B.1 of the NRC Enforcement Policy.

IV. PLANT SUPPORT

R1

Radiological Protection and Chemistry (RPRC) Controls

R1.1

Im lementation of the Radiolo ical Environmental Monitorin

Pro ram 84750

'ns

ection Sco

e

The inspectors observed

and assessed

the licensee's capability to implement the

radiological environmental monitoring program (REMP), The inspectors reviewed the

REMP procedure manual, visited selected sampling locations to confirm that

samples were being obtained from the locations specified in the Offsite Dose

Calculation Manual (ODCM), witnessed licensee and contractor personnel

exchange

air filters and charcoal canisters, examined the air samplers to determine operability

and calibration status, and reviewed the results of the Land Use Census.

The above

areas were inspected against specific TS requirements

Sections 3/4.6.20, 3/4.6,21,

3/4.6.22 for Unit 1 and Sections 3/4.12.1, 3/4.12.2, and 3/4.12.3 for Unit 2, the

ODCM, and the UFSAR.

b.

Observations

and Findin s

The environmental protection group, part of the Licensing/Environmental

Department at Nine Mile Point, has the responsibility to implement the REMP in

cooperation with the J. A. FitzPatrick Radiological Environmental Services

Department.

Environmental samples were collected by licensee and contractor

personnel

(Ecological Analysts Science and Technology) and were analyzed at the

FitzPatrick Environmental Laboratory (JAFEL).

The sampling stations included air samplers for airborne iodines and particulates,

a

composite water sampling station (control station), a milk farm, vegetation

locations, and several thermoluminescent

dosimeter (TLD) stations for measurement

of direct ambient radiation.

The inspectors witnessed the weekly exchange of

14

charcoal cartridges and air particulate filters at selected sampling stations.

All

observed

air sampling equipment was operational and calibrated at the time of the

inspection.

The TLDs were placed at the designated

locations as specified in the

ODCM. Milk and vegetation samples were obtained from the locations specified in

the ODCM. Sample collection was performed according to the appropriate

procedures.

The REMP procedures

contained

all the guidance necessary to collect and prepare

environmental sample media.

The procedures

included air, milk, water sampling

methods, dry gas meter calibration calculations for the air samplers,

and a method

for conducting the Land Use Census.

The procedures

were of good technical

content, concise,

and provided the required direction and guidance for implementing

an effective REMP.

C.

Conclusions

Based on the above review, direct observations,

discussions with personnel,

and

examination of procedures,

the inspectors determined that the licensee continued to

effectively implement the REMP in accordance

with the TS, ODCM, and UFSAR

commitments.

R1.2

'eteorolo

ical Monitorin

Pro ram 84750

Ins ection Sco

e

The inspectors observed

and evaluated the licensee's meteorological monitoring

program (MMP) to determine w'hether the instruments

and equipment were

operable, calibrated, and maintained.

The MMP was inspected against TS

requirements Section 3/4.7.3 for Unit 2, Section 2.3 of the UFSAR, and Regulatory

Guide 1.23.

b.

Observations

and Findin s

The Meteorological Services group continued to have oversight for the MMP; and

the ISC department continued to maintain all sensors at the main, backup, and

inland towers for the Nine Mile Point/FitzPatrick site and perform calibrations in

accordance

with Unit 2 TS requirements.

The calibration procedures

were available

and implemented for wind speed, wind direction, temperature

sensors,

and other

related components.

The inspectors reviewed the most recent semi-annual

calibration results for the above parameters

and noted that the calibrations were

adequately performed in accordance

with the appropriate IKC procedures.

All

reviewed calibration results were within the licensee's

acceptance

criteria. The

FitzPatrick INC department calibrated the strip chart recorders

in accordance

with

the licensee's calibration schedule.

The results were within the licensee's

established

acceptance

criteria.

The inspectors observed the sensors

and the associated

outputs in the computer

building, as well as the outputs in the Nine Mile control room and Technical Support

15

Center.

Accurate meteorological data were available't each location using digital

display from the system computer and analog strip chart recorders.

Conclusion

Based on the above review, direct observations,

discussions with personnel,

and

examination of procedures

and records for calibration of equipment, the inspectors

determined that the licensee continued to effectively implement the MMP in

accordance

with the Unit 2 TS, UFSAR commitments,

and Regulatory Guide 1.23.

RP&C Organization and Administration

Or anization Chan

es and Res

onsibilities 84570

Ins ection Sco

e

The inspectors reviewed any organization changes

and the responsibilities relative to

oversight of the REMP and MMP since the previous inspection conducted

in June

1995, to verify the implementation of the TS requirements.

Observations

and Findin s

The inspectors identified changes

in the organizations

responsible for the REMP and

MMP.

In October 1995, the Environmental Protection-Radiological;

Technical

Services Branch was transferred to the Licensing Branch and subsequently

renamed

the Licensing/Environmental

Branch.

The Environmental Protection-Meteorological;

Technical Services Branch was relocated to the Emergency Preparedness

Department and subsequently

renamed Meteorological Services.

The Environmental

Protection Coordinator-Radiological

continued to implement the REMP and report to

the Supervisor,

Environmental Protection, who reports to the Manager,

Licensing/Environmental

Branch.

Meteorological Services continued to have

oversight of the MMP. The Meteorological Services Coordinator reports to the

Emergency Preparedness

Director, who reports to the Manager, Nuclear Training

Branch.

Conclusion

Based on the above review, the inspectors did not identify any negative impact on

the'implementation of the REMP and MMP and confirmed that the responsible

personnel

in these programs essentially remained the same.

Annual Environmental 0 eratin

Re ort 84570

Ins ection Sco

e

The inspectors reviewed the Annual Environmental Operating Report to verify the

implementation of the TS requirements

Section 6.9.1.d. for Unit 1 and Section

6.9.1.7 for Unit 2.

16

Observations

and Findin s

The inspectors reviewed the Annual Radiological Environmental Operating Report for

timely reportability and the results of the routine analysis of REMP samples

and

quality assurance

results.

The Annual Radiological Environmental Operating Report

for 1995 provided a comprehensive

summary of the analytical results of the REMP

around the Nine Mile Point site and met TS reporting requirements.

No obvious

omissions,

anomalous data or trends were identified.

c.

Conclusion

Based on the above review, the inspectors determined that the licensee maintained

good management

control to implement the TS requirements with respect to the

Annual Radiological Environmental Operating Report.

R7

Quality Assurance in RP5C Activities

R7.1

Qualit

Assurance Audit Re orts 84750

a.

Ins ection Sco

e

The inspectors reviewed the Quality Assurance

(QA) audit report against criteria

contained in TS requirements,

Section 6.5.3.8.i for both units.

b.

Observations

and Findin s

The nuclear QA audit 95019, "Environmental Protection/REMP and Radioactive

Effluents," was performed December 4-8, 1995, and included an assessment

of the

REMP and MMP. The audit was conducted

by the nuclear QA audit group and

technical specialists.

The scope and technical depth of the audit were good and

effectively assessed

the programs for strengths

and weaknesses.

The audit scope

also included an assessment

at the JAFEL.

Few findings and recommendations

were identified.

The responsible

departments

responded

to these findings and

recommendations

in a timely manner.

C.

Conclusions

Based on the, above review, the inspectors determined that the licensee conducted

an audit of sufficient technical scope and depth to adequately

assess

the quality of

the REMP and MMP, as required by the regulatory requirements.

R7,2

Qualit

Assurance of Anal tical Measurements

84750

Ins ection Sco

e

The inspectors reviewed the licensee's

QA program for analytical measurements

of

radiological environmental samples including the Interlaboratory Comparison

Program

(EPA Cross-check

Program) required by the TS and ODCM.

17

Observations

and Findin s

The quality control (QC) program for analysis of environmental samples was the

responsibility of the FitzPatrick Radiological and Environmental Services

(RES)

Supervisor at the JAFEL, located in Fulton, N.Y. The laboratory maintained internal

QA programs including environmental split samples,

spike samples,

and blind

samples.

Control charts for the gamma spectroscopy

counter, liquid scintillation

counter, and low background

counters were well maintained and calibrations were

performed as scheduled.

QA samples were analyzed according to the schedule.

The laboratory supplied reports of QC results to the Nine Mile Environmental

Protection Coordinator for data review and analysis.

When discrepancies

were

found, the Coordinator consulted with the RES Supervisor.

Reasons for the

discrepancies

were investigated

and resolved.

The inspectors reviewed the JAFEL

Quality Assurance

Reports for 1994 and 1995 which contained the results of the

QA programs.

All reviewed results were in agreement.

The laboratory participated in the EPA cross-check

Program.

The inspectors

reviewed the cross-check results for 1995 and noted that results were within the

EPA's acceptance

criteria.

In 1996, the licensee started to use a vendor laboratory

(Analytics, Inc.) to continue the interlaboratory comparison program since the EPA

stopped providing this service after December 1995.

The inspectors reviewed the

cross-check

results for the first quarter 1996, and noted that the results were

within the established

acceptance

criteria. The inspectors

also determined that the

program is equivalent to the EPA cross-check

Program.

JAFEL plans to use

Environmental Management

Laboratory (EML) to supplement the Analytics Program.

This program is expected to be implemented

in September

1996.

Since JAFEL also obtained calibration standards

from Analytics Inc., the inspectors

questioned if the samples provided for the intercomparison

program are independent

from the calibration standards.

Review of the Analytics Inc. program revealed that

independence

was assured

since Analytics Inc. established two separate

and

independent

programs, one for the calibration standards

and the other for the

intercomparison

program.

The inspectors observed

a chemistry technician prepare routine environmental milk

samples for counting.

The technician followed the procedure

and used good

laboratory practices.

The inspectors also reviewed the analytical results for 1996

(January - July) and noted that there were no anomalous

results.

Conclusion

Based on the above reviews and discussions,

the inspectors determined that the

licensee continued to implement a good quality assurance

program in accordance

with regulatory requirements.

P3

EP Procedures

and Documentation

18

P3.1

In-Office Review of Chan

es to the E-Plan

82701

A emergency

preparedness

specialist inspector conducted

an in-office review of

revisions to the emergency

plan and implementing procedures

(EPIPs) submitted by

the licensee.

The specific revisions reviewed follows. The inspectors determined

that the revisions did not reduce the effectiveness

of the emergency

plan and were

acceptable.

Procedure

No.

Title

Revision No.

EPIP-EPP-01

EPIP-EPP-02

EPIP-EPP-04

EPIP-EPP-05

EPIP-EPP-07

EPIP-EPP-08

EPIP-EPP-09

EPIP-EPP-1 0

EPIP-EPP-1 2

EPIP-EPP-13

EPIP-EPP-1 6

EPIP-EPP-1 7

EPIP-EPP-20

EPIP-EPP-22

EPIP-EPP-23

EPIP-EPP-24

EPIP-EPP-27

EPIP-EPP-30

Site Emergency Plan

Classification of Emergency Conditions

't

Unit 1

Classification of Emergency Conditions

at Unit 2

Personnel

Injury or Illness

Station Evacuation

Downwind Radiological Monitoring

Off-Site Dose Assessment

and Protective

Action Recommendation

Determination of Core Damage Under

Accident Conditions

Security Contingency Event

Re-Entry Procedure

Emergency Response

Facilities Activation

and Operation

Environmental Monitoring

Emergency Communications

Procedure

Emergency Notifications

Damage Control

Emergency Personnel Action Procedures

Nuclear Transportation Accidents

Emergency Public Information Procedure

Prompt Notification System Problem Response

34

6

2

1

2

6

3

1

5

1

5

1

2

1

V. Management Meetings

X1

Exit Meeting Summary

At periodic intervals, and at the conclusion of the inspection period, meetings were

held with senior station management

to discuss the scope and findings of this

inspection.

The resident inspector's final exit meeting occurred on August 30,

1996.

NMPC did not dispute any of the inspectors findings or conclusions.

The

preliminary exit for the radiological environmental monitoring and meteorological

monitoring inspection was conducted

on July 26, 1996.

19

Based on the NRC Region

I review of this report, and discussions with NMPC

representatives,

it was determined that this report does not contain safeguards

or

proprietary information.

X3

Management Meeting Summary

X3.1

Re ional Dro -In Visit b

Executive Vice President

On July 16, 1996, Mr. B. Ralph Sylvia, NMPC Executive Vice President and Chief

Nuclear Officer, met with Mr. T. Martin, Regional Administrator, Mr. W. Kane,

Deputy Regional Administrator, and Mr. R. Conte, Chief, Reactor Projects Branch

No. 5, at the NRC Region

I offices in King of Prussia, Pennsylvania.

The topics

discussed

were the status of the "Power Choice Option" for the state of New York,

in which power companies would individually compete in an open market for the

sale of electricity; and the NMPC response

to the NRC Notice of Violation and

Proposed

Imposition of Civil Penalty (dated June 18, 1996).

Mr. Sylvia also

provided a copy of the response

at that meeting.

20'ARTIAL

LIST OF PERSONS CONTACTED

Nia ara Mohawk Power Cor oration

R. Abbott, Vice President 5 General Manager - Nuclear

J. Aldrich, Maintenance

Manager, Unit 1

M. Balduzzi, Operations Manager, Unit 1

D. Barcomb, Radiation Protection Manager, Unit 2

C. Beckham, Manager, Quality Assurance

H. Christensen,

Nuclear Security Manager

J. Conway, Plant Manager, Unit 2

K. Dahlberg, General Manager - Projects

A. DeGracia, Work Control/Outage

Planning, Unit 1

R. Dean, Engineering Manager, Unit 2

G. Helker, Work Control/Outage

Planning, Unit 2

J. Jones,

Director, Emergency Preparedness

M. McCormick, Vice President - Nuclear Safety Assessment 5 Support

L. Pisano, Maintenance

Manager, Unit 2

N. Rademacher,

Plant Manager, Unit

1

P. Smalley, Radiation Protection Manager, Unit 1

R. Smith, Operations Manager, Unit 2

B. Sylvia, Executive Vice President - Nuclear

K. Sweet, Technical Support Manager, Unit 1

C. Terry, Vice President - Nuclear Engineering

R. Tessier, Nuclear Training Manager

K. Ward, Technical Support Manager, Unit 2

D. Wolniak, Licensing/Environmental

Manager

W. Yaeger, Engineering Manager, Unit 1

New York Power Authorit

- J. A. FitzPatrick

N. Avrakotos, Emergency Planning Manger

J. McCarty, Quality Assessment

Supervisor

A. McKeen, Radiological and Environmental Services Manager

21

INSPECTION PROCEDURES USED

IP 37551:

IP 40500:

IP 60705:

IP 61726:

IP 62703:

IP 71707:

IP 82701:

IP 84750:

IP 90712:

IP 92700:

IP 92901:

IP 92902:

IP 92903:

IP 92904:

On-Site Engineering

Effectiveness of Licensee Controls in Identifying, Resolving, and Preventing

Problems

Preparations

for Refueling

Surveillance Observations

Maintenance Observation

Plant Operations

Operational Status of the Emergency Preparedness

Program

Radioactive Waste Treatment, and Effluent and Environmental Monitoring

In-Office Review of Written Reports of Nonroutine Events at Power Reactor

Facilities

Onsite Followup of Written Reports of Nonroutine Events at Power Reactor

Facilities

Followup - Operations

Followup - Engineering

Followup - Maintenance

Followup - Plant Support

OPENED

50-41 0/96-07-01

50-410/96-07-02

50-41 0/96-07-03

50-410/96-07-04

50-410/96-07-05

50-41 0/96-07-06

50-220/96-07-07

50-220/96-07-08

50-410/96-07-08

50-220/96-07-09

50-410/96-07-09

50-41 0/96-07-10

50-220/96-07-1

1

50-410/96-07-1

1

50-220/96-07-1 2

50-410/96-07-1 2

50-41 0/96-07-1 3

50-220/96-07-1 4

50-410/96-07-1 4

50-410/96-07-1 5

50-220/96-07-1 6

50-220/96-07-1 7

50-410/96-07-1 7

50-220/96-07-1 8

50-410/96-07-1 8

50-220/96-07-1 9

50-41 0/96-07-1 9

CLOSED

NONE

22

ITEMS OPENED, CLOSED, AND UPDATED

URI

The mechanical seal on a feedwater pump was replaced

without a procedure.

URI

No incoming survey for a radioactive material shipment.

IFI

Weaknesses

in the DER proc'ess.

IFI

-

ISEG responsibilities associated

with the review of NRC

issuances.

IFI

Weaknesses

in the 50.59 safety evaluation process.

IFI

IFI

IFI

IFI

Long standing hardware problems uncorrected.

Unit 1 is unable to parallel the EDGs with offsite for

restoration after a loss of offsite power.

MIC control systems installed as temporary modifications

over 4 years ago.

Material conditions in several areas of the plant were poor.

IFI

Weaknesses

in the Emergency Preparedness

program.

VIO

The functions of the ISEG are not described

in written

procedures.

VIO

Two examples were identified of inadequate

procedures for

related to the EDG lube oil and fuel oil duplex strainers.

VIO

A UFSAR drawing for the core spray system was changed

without performing a 50.59 safety evaluation.

URI

Determine if the temporary change process was used to

change the intent of an operability test procedure.

URI

A procedure

included in a PMT package was changed after

issuance

of the work package, without changing the PMt.

URI

DERs identified several examples of inadequate

restoration of

systems after maintenance

or testing.

URI

Configuration control concerns due to DCRs were not in the

database.

URI

Post-job critique information was not incorporated into the

WC Mosse database.

URI

Several examples of lubrication program problems.

UPDATED

NONE

23

LIST OF ACRONYMS USED

ALARA

APRM

BWR

BWROG

CFR

CGID

cps

CRD

DER

DLA

DOT

dp

EPA

FB

FCV

FFD

FPP

ft'E

GEMS

GTS

IKC

IN

INPO

IR

IRM

ISEG

ISI

LCO

LER

LPRM

MCPR

MMP

MSIV

NCV

NMPC

NOV

NRC

NRR

ODCM

PIP

psia

pslg

QA

RBM

As Low As Reasonably

Achievable

Average Power Range Monitor

Boiling Water Reactor

Boiling Water Reactor Owners Group

Code of Federal Regulations

Commercial Grade Item Dedication

counts per second

Control Rod Drive

Deviation/Event Report

Dynamic Learning Activities

Department of Transportation

differential pressure

Environmental Protection Agency

Fire Brigade

Feedwater Control Valve

Fitness for Duty

Fire Protection Program

square feet

General Electric

Gaseous

Effluent Monitoring System

Standby Gas treatment System

Instrument and Controls

Information Notice

Institute of Nuclear Power Operations

Inspection Report

Intermediate Range Monitor

Independent

Safety Engineering Group

In-Service Inspection

Limiting Condition of Operation

Licensee Event Report

Local Power Range Monitor

Minimum Critical Power Ratio

Meteorological Monitoring Program

Main Steam Isolation Valve

Non-Cited Violation

Niagara Mohawk Power Corporation

Notice of Violation

Nuclear Regulatory Commission

Office of Nuclear Reactor Regulation

Offsite Dose Calculation Manual

Position Indicator Probes

pounds per square inch absolute

pounds per square inch gage

Quality Assurance

Rod Block Monitor

24

LIST OF ACRONYMS USED

(continued)

RCA

RCS

REMP

RFO

RP

RPRC

RPM

RPS

RRP

RWP

SE

SFC

SIL

SIT

SORC

SRAB

SRM

SRV

SSS

TSSR

UFSAR

URI

VDC

VIO

WO

Program

equire ment

Radiologically Controlled Area

Reactor Recirculation System

Radiological Environmental Monitoring

Refueling Outage

Radiation Protection

Radiation Protection and Chemistry

Radiation Protection Manager

Reactor Protection System

Reactor Recirculation Pump

Radiation Work Permit

Safety Evaluation

Spent Fuel Pool Cooling

Service Information Letter

Special Inspection Team

Station Operations Review Committee

Safety Review and Audit Board

Source Range Monitor

Safety Relief Valves

Station Shift Supervisor

Shift Technical Assistant

Thermoluminescent

Dosimeter

Technical Specification

Technical Specification Surveillance

R

Update Final Safety Analysis Report

Unresolved Item

Volts Direct Current

Violation

Work Order

ATTACHMENTA

RESULTS OF THE REVIEW OF NRC IPAP

IR 50-220/96-201

AND 50-410/96-201:

LIST OF VIOLATIONS,

UNRESOLVED ITEMS, AND INSPECTOR FOLLOWUP ITEMS

'

The review of the results of the NRC Integrated Performance Assessment

Process

(IPAP)

Inspection Report 50-220/96-201

and 50-410/96-201

identified violations (VIO) and

unresolved items (URI). Some items identified by the IPAP were previously identified or

addressed

earlier inspection reports and are annotated

as such.

The details are contained

in the IPAP inspection report (IR), below is a summary of the issues identified for further

review:

1

~

(IR Section

1

~ 1) The responsibilities of the independent

safety engineering

group

(ISEG) are specified in the Unit 2 TSs.

The functions of ISEG are described

in the Unit

2 UFSAR, which discusses

that the establishment

of the ISEG is in response to the

requirements of NUREG-0737.

However, the team identified that there were no

procedures for the implementation of ISEG activities.

This is a violation of TS 6.8.1.b,

which requires written procedures

be established

and implemented to cover the

activities that implement the requirements of NUREG-0737.

(VIO 50-410/96-07-01)

2.

(IR Section 2.4) At the time of the inspection,

a procedure

upgrade program was in

progress at Unit 2 to address

problems identified in operations procedures.

The team

identify the following discrepancies:

~

The Division I and II EDG turbo lube oil duplex filter was aligned to the "BOTH"

position, based on the vendor technical manual guidance; this was in accordance

with the procedure (N2-OP-100A, Revision 5, "Standby Diesel Generators" ).

However, the team identified that the alarm response

portion of procedure

N2-OP-

100A for annunciator "Lube Oil Low Pressure Turbo" directed the operator to

swap over to the standby filter. With the filter aligned to "BOTH", there would be

no standby filter available; thus, the alarm response

procedure action could not be

performed.

~

The Division II EDG fuel oil duplex strainer was aligned such that both strainer

elements were in service.

The operating procedure

(N2-OP-100A) stated that

operation with the selector lever in the "MID"or "BOTH" position should only be

considered

if the EDG would otherwise be inoperable.

However, the selector lever

in the "BOTH" position while the EDG was operable.

Furthermore, the valve line-

up in the procedure

noted that the position of the selector lever should be "as

selected."

These represent

a violation of the Unit 2 TS, Section 6.8.1, in that procedures

were

not adequately

established

or implemented.

In addition, the above are examples of

conflicting requirements within procedures

and are indicative of an inadequate

procedure review process.

(VIO 50-410/96-07-02)

3.

(IR Section 3.3)

Unit 1 design change (SC1-0056-91) required a revision to UFSAR

Figure X-6 to change the position of the service water system screen wash pump

header inter-tie valves from normally open to, normally closed and to delete an

incorrectly shown valve.

No safety evaluation was performed because,

in the

preliminary evaluation (No. D93-113), the responsible

engineer documented that the

UFSAR was not affected because

descriptions

in the UFSAR were not changed.

The

team ascertained

that the engineer incorrectly characterized

this as an editorial change

A-1

to the UFSAR figure. The preliminary evaluation was not in compliance with

licensee's

procedure

NIP-SEV-01, "Applicability Reviews and Safety Evaluations,"

which di'd not allow minor configuration changes to UFSAR figures to be considered

as

editorial corrections.

The failure to complete the safety evaluation as required for

changes

in the facility as described

in the UFSAR is a violation of 10 CFR 50.59.

(VIO

50-220/96-07-03)

(IR Sections 2.1 and 2.2) During a review of DER 1-95-0957, the team noted that

temporary changes

were made to a Unit 1 procedure

(N1-ST-Q1B, Revision 4, "Core

Spray Loop 12 Pumps and Valves Operability Test" ) as a part of modification N1-90-

041.

This item is unresolved

pending further NRC review to determine if the

temporary changes

altered the intent of the procedure.

(URI 50-220/96-07-04)

(IR Section 2.2)

DER 1-95-1945 documented

that a procedure for post-maintenance

test (PMT) of the reactor building track bay door was revised after the work package

was issued, the revised procedure deleted some testing requirements for the door.

The operations

personnel performing the PMT were not aware of this revision.

This is

an URI pending an evaluation to determine the adequacy of the PMT performed for the

reactor building track bay door, and to evaluate the work control process for

appropriate barriers in place to prevent recurrence of similar problems.

(URI 50-220/96-07-05)

(IR Sections 2.3 and 4.2) The review of Unit 2 DERs indicated work control problems

involving restoration of systems

and components following maintenance

or testing.

For example:

an RHR pump minimum flow valve was inadvertently left shut following

a surveillance

(DER 2-94-1612); an isolation cooling system steam line drain pot level

switch variable leg isolation valve was incorrectly left shut following repacking

(DER

2-95-0237); and one train of suppression

chamber spray was disabled due to failure

to properly restore the correct valve line up following a leakage test (DER 2-95-1854).

Furthermore, the team reviewed 87 recent work packages,

and noted that mechanical

work packages

did not include a sign-off step at the end of the package to confirm

that configuration control was maintained, nor was restoration clearly documented

and

signed off in the text. This is an URI to evaluate the issues described

in the subject

DERs, whether the corrective actions taken to address

each DER were appropriate,

and to evaluate the adequacy of NMPC's controls for configuration restoration

following maintenance

or testing.

(URI 50-410/96-07-06)

(IR Section 3.2)

DERs 1-95-2051

and 1-95-1075 documented

configuration control

concerns

in electrical drawings, because

design change requests

(DCRs) initiated

several years ago were not entered

in the configuration control database.

Also,

drawings in other disciplines were noted as being affected.

This is an URI to

determine the significance of the configuration control issues documented

in the

DERs, to review the timeliness and adequacy of the corrective actions identified in

each DER.

(URI 50-220/96-07-07)

(IR Section 4.1)

The team identified that the information from post-job critique forms

was not consistently entered into the work control database

(W C Mosse).

This is an

A-2

URI to determine the procedural requirements

associated

with the post-job evaluation

and the incorporation of the critique information into the WC MOSSE database.

(URI 50-220/96-07-'08 & 50-4'I0/96-07-08)

9.

(IR Sections 2.2 and 4.3)

Lubrication program problems continued to occur at both

units:

DER 1-95-2181 documented

an error made in adding oil to Unit 1 CRD pump

¹12 bearing; DER 2-95-2848 documented

several instances of delays in preventive

maintenance

lubrication of pumps and motors at Unit 2; and DER 1-96-0739

documented that SDC pumps ¹11 and ¹13 had the motor bearing oil added to the

pump bearing and vice versa.

This is an URI to evaluate the adequacy of the

lubrication programs; the adequacy of corrective actions to address

previously

identified lubrication concerns;

and if the specific issues have been corrected,

(URI 50-220/96-07-09 & 50-410/96-07-09)

10.

(IR Section 4.5)

The mechanical seal replacement for the Unit 2 feedwater pump was

performed without a procedure,

although the work was done by a specially trained

maintenance

crew. This is an URI to determine if this practice is allowed by NMPC

procedures.

(URI 50-410/96-07-10)

(IR Section 5.2.1)

NMPC failed to conduct an incoming survey on a radioactive

material shipment.

This is an URI to determine if the failure to conduct the survey

violates NMPC procedures.

(URI 50-220/96-07-11

& 50410/96-07-11)

In addition to the violations and unresolved

items noted above, the IPAP report noted

several weaknesses.

These are listed below with an inspector follow item (IFI) number to

facilitate administrative tracking to closure.

12.

(IR Sections

1.2, 1.3, 2.2, and 4.2) Weaknesses

in the DER process were identified in

the areas of trending, root cause analysis, adequacy of corrective actions to prevent

recurrence,

and root cause analysis training. Also, the implementation of corrective

actions associated

with self-assessments,

ISEG, and QA recommendations

was not

verified sufficiently to assure that the required actions were effective,

For DER

2-95-1850, the root cause was a re-statement of the problem, the corrective actions

only narrowly addressed

the condition and did not address the cause.

(IFI 50-

220/96-07-1 2 & 50-410/96-07-1 2)

13.

(IR Section 1.1) The team identified that the ISEG responsibilities of reviewing NRC

issuances

(generic letters, bulletins, and information notices) was being performed by

other groups.

Except for issues of high interest, ISEG did not systematically review

NRC issuances

nor performed technical audits of their implementation by line

organizations.

(IFI 50-410/96-07-13)

14.

(IR Section 1.2) The team concluded that weaknesses

exist in the safety evaluations

completed by the licensee.

(IFI 50-220/96-07-14 & 50-410/96-07-14)

15.

(IR Section 3.2)

The team noted long-standing

hardware problems at Unit 2, such as

the loose parts monitoring.system, emergency

diesel generator air start system, and

A-3

standby gas treatment system.

The loose parts monitor issue was previously

identified as URI 50-410/95-25-02.

(IFI 50-410/96-07-15)

16.

(IR Section 2.4)

Due to the plant design, Unit 1 cannot perform a parallel transfer of

loads from the EDG to the offsite power source.

This will remain an IFI pending NRC

evaluation of the design adequacy.

(IFI 50-220/96-07-16)

t

17.

(IR Section 3.2) The temporary modification, at one of the units, for the

microbiologically induced corrosion control system for the service water system was

installed four years ago.

The temporary modification is still in service.

THE NRC

needs to evaluate the basis for the extended

installation period for the temporary

modification and plans to remove or make the modification permanent.

(IFI 50-220/96-07-17 & 50-410/96-07-17)

18.

(IR Sections 2.2 and 4.3)

Material condition discrepancies

were identified in the

rooms for the Unit 2 EDGs, the Unit 2 chilled water pumps, and the Unit 1 SDC

pumps.

(IFI 50-220/96-07-18 & 50-410/96-07-18)

19.

(IR Sections 5.3.3)

Many of the weaknesses

in the emergency preparedness

program

were related to changes

made in the EP program some time ago.

(IFI 50-220/96-07-

19 & 50-410/96-07-19)

20.

(IR Section 2.1)

LER 95-06 for Unit 2 reported the inadvertent disabling of a residual

heat removal (RHR) system suppression

chamber spray loop due to mispositioning of a

manual block valve.

During the time period that the loop was disabled, two mode

changes were made in violation of Technical Specification 3.0.4.

The LER was

reviewed in IR 50-410/95-23, and was identified as a non-cited violation.

21.

(IR Section 3.2) The IPAP team noted that DER completion dates for the corrective

and preventive actions were revised without justification. This issue was previously

identified as URI 50-410/95-25-03.

22.

(IR Section 5,3,1)

The IPAP team noted continuing incidents where personnel

had not

adhered to site radiological work control procedures

and practices.

This issue was

previously identified as VIO 50-220/96-06-05, 50-410/96-06-05."

23.

(IR Section 5.3.2)

The licensee had implemented appropriate corrective actions for

weaknesses

in the performance of security functions, such as unintentional disclosure

of safeguards

information in.a public document and a visitor entering the protected

area without a proper escort.

These issues were previously identified as URI 50-

220/94-13-03, 50-410/94-15-03

and VIO 50-410/94-18-02.

A-4