LER-1978-035, Forwards LER 78-035/01T-0 |
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REGULATORY FORMATION DXSTRXBUTXON TEM DOCKET NBR: 50 22p NINE M LE PT 1
RECXPIENT:
IER B.H DOC DATE:
781102 ACCESSION NBR: 7811p9p2 1
COPXES RECEIVED:
LTR 1
ENCL 1
ORIGINATOR:
HNEXDER COMPANY NAME: NIAGARA MOHAWK PWR
SUBJECT:
~
SIZE-1+4 LER478-035/01T<<O on 781020:all main steam hi h. flow xessure i;ndJc tin instr were found w set oints less than Tech 'S ecs, Herse "0&00 PSXG test ua e calibrated s used in test had loose screw s was recaliibrated, DI SQRISUTION CODE t
$ 002 DISTRIBUTION TITLEt.
INCIDENT REPORTS NOTARIZED ENCL?
BR F
W/a ENCL W/ENCL C
&DR W/ENCL I
8 H/2 ENCL MIPC W/3 ENCL I
8 C
SYSTEMS BR W/FNCL
, NOVAK/CHEC<
W/ENCL
- EEB W/ENCL t AD FOR ENG W/ENCL PLANT SYSTEMS BR W/ENCL HANAUFR W/ENCL AD FORPLANT.SYSTEMS W/ENCL AD FDR SYS 8
PROJ W/ENCL REACTOR SAFETY BR W/ENCL ENGINEERING BR W/ENCL KREGER/J, COLLINS W/ENCL POWER SYS
.BR W/ENCL E. Jordan W/ENCL LPDR W/ENCL NSIC W/ENCL
" ACRS W/t6 ENCL TOTAL NUMBER OF COPIES REQUIREDt LTR ENCL FOR ACTION ORB03 BC go) 74,. 1%a NOTES: HEAD TO HEAD
T 1
NMP-1064 NIAGARAMOHAWKPOWER CORPORATION/300 ERIE BOULEVARDWEST, SYRACUSE, N.Y. 13202/TELEPHONE (315) 474-1511 November. 2, 1978 A,. Boyee H. G/Lie/L NJLecto/L Unacted S~ee hfueLea/L ReguLato/Ly Comm@ amn Region 7
631 Pa/ck Avenue, King of Purana, PA.
19406 RE:
Socket hlo. 50-220 LER 78-035/01T-0 h
1 7n acco/cdance with Nne h4Le Point hlueLea/L S~on 0+0'ill TechnicaL Spmipeatimv.,
uIe he/Leby aubnkt Licensee Event Repo&,
LER 78-95, which m in v~Lation o$ Section 9.6.2b of Che Tech'.eaL Speci P.cation'.
TkQ /Lepo/Lt ulnae compLeted in Che (o/Imat designated in hlUREG-0161, dated JuLy 1977.
Since/ceLy, Original signed by R.R. Schneider R.R. Schneide/L t/ice Paae&ent-ELect/1ie Production Attachments (3 copiu) xc:
Omecto/L, 0)pce o( 78E (40 copie5)
Mcecto/L, 0(pce o( h(7PC (9 copiu)
I7.77)
CONTROL BLOCK:
I N
Y N
M P
[OD1]
CON'T 7
8 9
LICENSEE CODE 1O20 0
14 15 LICENSEE EVENT R EPORT Q
1
{PLEASE PRINT YPE ALLREQUIRED INFORMATION) 6 0
0 0
0 0
0 0 Q24 1
1 1
1 05~05 LICENSE NUMBER 25 26 LICENSE TYPE 30 57 CAT 58 7
8
~oz 8Q81 1
0 1
7 8
QB 74 75 REPORT DATE 80 eight main steam high flow pressure indicating instruments with set-QBO 5
0 0
0 2
2 OQ7 1
0 2
0 60 61 DOCKET NUMBER 68 69 EVENT DATE EVENT DESCRIPTION AND PROBABLE CONSEQUENCES QIO Durin stead state o eration, erformance of Nl-ISP-RE22 found all 4
points less conservative than T.S. 3.6.2b Subsequent investi a'tion,
~os
~OB recalibration, and retesting indicated that only three instruments were less conservative and that test au e was inaccurate since nre-vious cal.
on 10-10-78.
Condition has minimal safety implications.
~OB 7
8 7
8 0
Other instrumentation would initiate same response.
80 9
SYSTEM
CAUSE
CAUSE COMP.
VALVE CODE CODE SUBCODE COMPONENT CODE SUBCODE SUBCODE
~CC Q11 E
Q12
~EQ13 I
N 5
T R
U QE
~XQ15
~Z 016 9
10 11 12 13 18 19 20 SEQUENTIAL OCCURRENCE REPORT REVISION LERIRO EVENT YEAR REPORT NO.
CODE TYPE NO.
017 REPoRT ~25 U
L0035 Qr
~01 QT U
Lot 21 22 23 24 26 27 28 29 30 31 32 ACTION. FUTURE EFFECT SHUTDOWN ATTACHMENT NPRDP PRIME COMP.
COMPONENT TAKEN ACTION ON PLANT METHOD HOURS 022 SUBMITTED FORM SVB.
SUPPLIER MANUFACTURER QIB ~GO)9
~ZO20 HO2'023
~NO24
~Ozs H
1 Ozs 33 34 35 36 37 40 41 42 43 44 47 CAUSE DESCRIPTION AND CORRECTIVE ACTIONS Q2I A Heise 0-200 PSIG test gauge was calibrated and used in the surveil-4 lane'e tests.
Subsequently, it was found to have a loose screw inter-nally, and recalibrated.
RE22s were retested and all were readjusted.
Procedure
- changed, establishing setpoint guide value of 100 PSID +/-2; PSID.
LBJQ>>
s E
Qss
~09 2
Q26 NA 7
8 9
10 12 13 44 ACTIVITY CONTENT RELEASED OF RELEASE AMOUNTOF ACTIVITYQ
~l6
~2 P>>
2 Q24 NA 7
8 9
10 11 44 PERSONNEL EXPOSURES NUMBER TYPE DESCRIPTION OSB 7 ~00 0
QET Z
Qss NA 7
8 9
11 12 13 PERSONNEL INJURIES 7
8 9
11 12 LOSS OF OR DAMAGETO FACILITYQ43 TYPE
DESCRIPTION
B N
Q42 NA 8
9 10 PUBLICITY 7
8 9
10 45 46 NA 45
'7 8 1 'I 0 9 0
/1'ennis K. MacIjtittie NAME OF PREPARER 7
8 9
FACILITY
~30 METHOD OF STATUS 55 POWER OTHER STATUS Q DISCOVERY LOCATION OF RELEASE Q 80 80 80 80 80 80 NRC USE ONLY 68 69 <<0-139 80 Fr 0L0 DISCOVERY DESCRIPTION Survei1 lance Test
NIAGARAMOHAWKPOWER CORPORATION/300 ERIE BOULEVARDWEST, SYRACUSE, N.Y. 13202/TELEPHONE (315) 474-1511 Novembe/L 1, 1978
~. Boyce H. G~e/1.
Mn,ecto/L United S~es NucLeo/L ReguLatoay CommLw~on Region I 631 Parck Avenue N,ng o( Ptcussm, PA.
19406 RE:
'Oocket No.
50-220 LER 78-035/01T-O Nme IKLe Pet NucLean, S~on Unit <1 8~ hh,.
Gru.en,:
8uning steady a~e ope/ation, pe/L)ordnance o) Nl-ISP-RE22 (ound aLL eight prcesame ~nNcating a~ches IoMh a&points Less conse/1vative Chan
+Mowed bg TechIM'caL Spec4gcation 3.6.2b.
Thee speci +~on aequutes a aetpo~ o) Less Chan o/1. equaL Co 105 pate +/-1 ps&.
The. hku,n Steam Line. H~h FLow aetpokns uIwe found and Le(4 at We
)oLLoeurg vaLues on Octobe/1. 20, 1978:
- - Insolent
~Pd t
Let
(
~dj RE22A RE228 RE22C RE22'0 RE22E RE22F RE226 RE22H 107.0 107. 0 106. 5 108. 0 106.2 108. 5 108. 5 107. 5 104. 5 105. 0 105. 0 105. 0 105. 0 104. 5 104. 5 105. 0 A eever of Che RE22 Su/LveLMance Test /deco/1ds ~n&cated ~ a cpu.$4 as Large as found ~n~ ~nsWnce uIas ~e fo/L one ~jument, and had nevm occ~ed on aLL eight.
In adcKtion, Che HeLee 0-200 pa~g Zest gauge 10as caEL b/1ated on Octobe/L 10, 1978 and (ound Co have, been ~n e/1/co/L.
As a p/1ec~n, &e H~e gauge, uIas zecaDb/1ated, and Che am-veiLLance CesC /I.epeated on 0&obe/1. 27, 1798.
The RE22'6 Nerve found at Che /olloeing aetpoi~:
Found
( aid)
RE22A RE228 RE22C RE220 RE22E RE22F RE22G RE22H 109. 0 109. 5 109. 5 103. 0 109. 0 103. 5 103. 0 109. 5 V~ng Che one, (reek b~een CuW, M m kcghly ueLRely Chat all
~e~
twould again have cpu.(ked an average o$ 1.5 paid (Whee ~e a mob,e conservative %Rection).
Tlute apparent change, ~n 6&point'L6 being ~bMed Co a loose aecev found intercnaMy dkuu.ng She Scud caL-ib~on.
%fuming Chat CheinMial eve em cawed by a tut gauge, ceading 1.5 prig Sigh, Che comected "found" and 'le)4" value Joe We 0&obm 20, 1978 '4uA me ae (olloes:
RE22A RE228 RE22C RE2 217 RE22E RE22F RE22G RE22H CoM,ected
~Fd t
'dt 105. 5 105. 5 105. 0 106. 5>>
104.7 107.0" 107.0*
106.0 CoMect'ed Le 4
( aid) 103. 0 103. 5 103. 5 103. 5 109. 5 103. 0 103. 0 103. 5 "Co~y Co Techie,cd Speci,+cation 9.6.2b The cpu'.$A noCed on Cfvcee im~e~
alee mme in Zine~ Mends MWbMshed ovn Ae Lask Zen montM.
Tk@ condition /A nu.mmal safety knpWeatioes be~e only one. oLt o$
$om i,me~~
mme ~pLn exch channel 4o an~ate WSIV closure, and Pve o4hm iruWume~ mould have functioned.
In Che eve 'Chat aK eight ~ne~mt (vere, in (act, lpga comm-vative, CRee oWw ~m~eet ayah~
(Lotv Cond~M Vacuum, Main Steam Line H~gh Ra~on, and Wain Steam Line High Temple) tvould have.
ed Che MSIV closure.
Pcocedurcu have, been changed Xo uWbMh a gLide vaQce o$
100 paid
+/-2 paid Joe She aetpoint when pn$ orcming Nl-ISP-RE22.
TkQ, eLLLp~
ine~ent cM$A o$ Che mageQ'+de exp',enced, tvLthoM degrading She hyhCem'4 JLchpoKhe.
VMy~y you/eh, Original Signed by R.R. Schneider R.R. Schneidetc Vice Pauident-Ele~c Production
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| 05000220/LER-1978-001, Submittal of Licensee Event Report LER 78-01 Concerning Delta Temperature of the Discharge Water Exceeded Environmental Tech. Spec | Submittal of Licensee Event Report LER 78-01 Concerning Delta Temperature of the Discharge Water Exceeded Environmental Tech. Spec | | | 05000220/LER-1978-003, Regarding Drywell High Pressure Switch RE04A Setpoint Drift and LER 78-003-00 | Regarding Drywell High Pressure Switch RE04A Setpoint Drift and LER 78-003-00 | | | 05000220/LER-1978-005, And LER 78-005-00 for Nine Mile Point, Unit 1 Re During Unit Shutdown, Reserve Power Breaker on Power Board II Failed to Close in After Loss of Normal Power and During Plant Outage While Marking Up Outside MSIV 01-03 Discovered | And LER 78-005-00 for Nine Mile Point, Unit 1 Re During Unit Shutdown, Reserve Power Breaker on Power Board II Failed to Close in After Loss of Normal Power and During Plant Outage While Marking Up Outside MSIV 01-03 Discovered That Valve | | | 05000220/LER-1978-006, Re During Steady State Operation, Performance of Surveillance Test IC-75 Found a Trip Setpoint of 22.5 Inches Water on One Vacuum Switch in the Vacuum Relief System from the Pressure Suppression Chamber to the | Re During Steady State Operation, Performance of Surveillance Test IC-75 Found a Trip Setpoint of 22.5 Inches Water on One Vacuum Switch in the Vacuum Relief System from the Pressure Suppression Chamber to the | | | 05000220/LER-1978-009-01, For Nine Mile Point Unit 1 Regarding Replacement of Explosive Charges in the TIP Shear Valves with New Charges and the Resulting Unsatisfactory Ohmmeter Continuity Test for Acceptable Electric Contact | For Nine Mile Point Unit 1 Regarding Replacement of Explosive Charges in the TIP Shear Valves with New Charges and the Resulting Unsatisfactory Ohmmeter Continuity Test for Acceptable Electric Contact | | | 05000220/LER-1978-009, And LER 78-010-00 for Nine Mile Point, Unit 1 Re Technical Specification Violations of Listed Sections | LER 78-009-00 and LER 78-010-00 for Nine Mile Point, Unit 1 Re Technical Specification Violations of Listed Sections | | | 05000220/LER-1978-013, And LER 78-013-00 for Nine Mile Point, Unit 1 Re Technical Specification Violations of Section 3.6.2 | And LER 78-013-00 for Nine Mile Point, Unit 1 Re Technical Specification Violations of Section 3.6.2 | | | 05000220/LER-1978-014, LERs 78-014,00, 78-016-00, and 78-016-00 for Nine Mile Point Unit 1 Regarding, Respectively, Discovery That the Fuel Transfer Pump on 102 D/G Would Not Fill the Day Tank, Discovery of RE18C with a Setpoint of 129 Inches Wc, and | LERs 78-014,00, 78-016-00, and 78-016-00 for Nine Mile Point Unit 1 Regarding, Respectively, Discovery That the Fuel Transfer Pump on 102 D/G Would Not Fill the Day Tank, Discovery of RE18C with a Setpoint of 129 Inches Wc, and RE04B | | | 05000220/LER-1978-015, And LER 78-015-00 for Nine Mile Point Unit 1 Regarding, Respectively, Discovery That the Fuel Transfer Pump in 102 D/G Would Not Fill the Day Tank and Discovery That 12 Control Room Air Treatment Fan Would Not Run | And LER 78-015-00 for Nine Mile Point Unit 1 Regarding, Respectively, Discovery That the Fuel Transfer Pump in 102 D/G Would Not Fill the Day Tank and Discovery That 12 Control Room Air Treatment Fan Would Not Run | | | 05000220/LER-1978-018, For Nine Mile Point Unit 1 Regarding Discovery of Main Steam High Flow Switch with a Setpoint of 106.2 PSI, Which Is Above the Technical Specification | For Nine Mile Point Unit 1 Regarding Discovery of Main Steam High Flow Switch with a Setpoint of 106.2 PSI, Which Is Above the Technical Specification | | | 05000220/LER-1978-019, For Nine Mile Point Unit 1 Regarding Discovery That Hydraulic Snubber 31-HS-1 Had Failed and Was Empty of Hydraulic Fluid and Disconnected from Its Anchor at the Feedwater Pipe | For Nine Mile Point Unit 1 Regarding Discovery That Hydraulic Snubber 31-HS-1 Had Failed and Was Empty of Hydraulic Fluid and Disconnected from Its Anchor at the Feedwater Pipe | | | 05000220/LER-1978-020, LERs 78-020-00, 78-021-00, 78-022-00, and 78-023-00 for Nine Mile Point Unit 1 Regarding, Respectively, Discovery of RE18A with a Setpoint of 135 Inches Wc, Discovery of RE04A and RE04B with a Setpoint of 3.65 PSIG, Discovery o | LERs 78-020-00, 78-021-00, 78-022-00, and 78-023-00 for Nine Mile Point Unit 1 Regarding, Respectively, Discovery of RE18A with a Setpoint of 135 Inches Wc, Discovery of RE04A and RE04B with a Setpoint of 3.65 PSIG, Discovery of Turbine . | | | 05000220/LER-1978-024, For Nine Mile Point Unit 1 Regarding Discovery That Test N1-St-Q2,4,5,7,8,9, and 10 Had Not Been Performed During a Review of Quarterly Surveillance Test Results | For Nine Mile Point Unit 1 Regarding Discovery That Test N1-St-Q2,4,5,7,8,9, and 10 Had Not Been Performed During a Review of Quarterly Surveillance Test Results | | | 05000220/LER-1978-025, LERs 78-025-00, 78-026-00, and 78-027-00 for Nine Mile Point Unit 1 Regarding, Respectively, Discovery of RE04D with a Setpoint of 3.70 PSIG, Discovery of Numerous Small Leaks in Small Sample and Instrument Pipes, and Discovery | LERs 78-025-00, 78-026-00, and 78-027-00 for Nine Mile Point Unit 1 Regarding, Respectively, Discovery of RE04D with a Setpoint of 3.70 PSIG, Discovery of Numerous Small Leaks in Small Sample and Instrument Pipes, and Discovery of RE22D Wit | | | 05000220/LER-1978-028, For Nine Mile Point Unit 1 Regarding Discovery of the Allowable Test Interval of TS 4.1.4c for the Core Spray Power-Operated Valves Had Been Exceeded | For Nine Mile Point Unit 1 Regarding Discovery of the Allowable Test Interval of TS 4.1.4c for the Core Spray Power-Operated Valves Had Been Exceeded | | | 05000220/LER-1978-029, Regarding Discovery of High Drywell Pressure Switches RE04A, RE04B, and RE04C with Setpoints Less Conservative than the Technical Specifications | Regarding Discovery of High Drywell Pressure Switches RE04A, RE04B, and RE04C with Setpoints Less Conservative than the Technical Specifications | | | 05000220/LER-1978-030, 78-031-00, and 78-032-00 for Nine Mile Point Unit 1 Regarding, Respectively, Unavailability of Feedwater Pump 29-03 While Its Pump Seals Were Replaced, Unavailability of Liquid Poison Pump NP02A While a Frozen Valve | 78-031-00, and 78-032-00 for Nine Mile Point Unit 1 Regarding, Respectively, Unavailability of Feedwater Pump 29-03 While Its Pump Seals Were Replaced, Unavailability of Liquid Poison Pump NP02A While a Frozen Valve | | | 05000220/LER-1978-033-03, /03L-0 on 780916:Surveillance Tests on Barton Model 289 Pressure Indicating Switches Showed Changes in Setpoints Due to Instru Drift.Rev Surveillance Test Scheds Now Adequate to Ensure Early Detection of Drifts | /03L-0 on 780916:Surveillance Tests on Barton Model 289 Pressure Indicating Switches Showed Changes in Setpoints Due to Instru Drift.Rev Surveillance Test Scheds Now Adequate to Ensure Early Detection of Drifts | | | 05000220/LER-1978-034, Regarding an Environmental Contractor Obtaining 22 Hourly Fish Impingement Samples, and One Two-Hour Sample, Which Is Contrary to the Technical Specification Requiring 24 Hourly Samples | Regarding an Environmental Contractor Obtaining 22 Hourly Fish Impingement Samples, and One Two-Hour Sample, Which Is Contrary to the Technical Specification Requiring 24 Hourly Samples | | | 05000220/LER-1978-035, Forwards LER 78-035/01T-0 | Forwards LER 78-035/01T-0 | | | 05000220/LER-1978-035-01, /01T-0 on 781020:all Main Steam High Flow Pressure Indicating Instr Were Found W/Setpoints Less than Tech Specs.Heise 0-200 PSIG Test Gauge Calibrated & Used in Test Had Loose Screw & Was Recalibrated | /01T-0 on 781020:all Main Steam High Flow Pressure Indicating Instr Were Found W/Setpoints Less than Tech Specs.Heise 0-200 PSIG Test Gauge Calibrated & Used in Test Had Loose Screw & Was Recalibrated | | | 05000220/LER-1978-036-04, /04T-0 on 781025:improper Appl of Brook Model 9456 Oval Gear Flowmeter Combined W/Failed Seal on Caustic Addition Pump Caused High Concentration of Sodium & Sulfate & Degraded Capability to Control Rate of Discharge | /04T-0 on 781025:improper Appl of Brook Model 9456 Oval Gear Flowmeter Combined W/Failed Seal on Caustic Addition Pump Caused High Concentration of Sodium & Sulfate & Degraded Capability to Control Rate of Discharge | | | 05000220/LER-1978-036, Forwards LER 78-036/04T-0 | Forwards LER 78-036/04T-0 | | | 05000220/LER-1978-037, Forwards LER 78-037/03L-0, 78-038/03L-0 & 78-039/03L-0 | Forwards LER 78-037/03L-0, 78-038/03L-0 & 78-039/03L-0 | | | 05000220/LER-1978-037-03, /03L-0 on 781027:test Revealed Trip Setpoint of 26.5 Inches Water on One Vacuum Switch in Vacuum Relief Sys from Pressure Supression Chamber to Rx Bldg.Caused by Instru Drift in a Mercoid Model CP4122 Vacuum Switch | /03L-0 on 781027:test Revealed Trip Setpoint of 26.5 Inches Water on One Vacuum Switch in Vacuum Relief Sys from Pressure Supression Chamber to Rx Bldg.Caused by Instru Drift in a Mercoid Model CP4122 Vacuum Switch | | | 05000220/LER-1978-038-03, /03L-0 on 781025:review of N1-ISP-RE22 Test Results Found 12 Instances Where Procedure Was Violated. Caused by Carelessness in Procedure Implementation. Re-instruction & Closer Supervision Instituted | /03L-0 on 781025:review of N1-ISP-RE22 Test Results Found 12 Instances Where Procedure Was Violated. Caused by Carelessness in Procedure Implementation. Re-instruction & Closer Supervision Instituted | | | 05000220/LER-1978-039-03, /03L-0 on 781103:surveillance Test N1-ISP-RE02 Revealed Rx Lo-Lo Water Level Switch W/Trip Setpoint of +2 Inches Water.Caused by Instru Drift.Setpoint Reset | /03L-0 on 781103:surveillance Test N1-ISP-RE02 Revealed Rx Lo-Lo Water Level Switch W/Trip Setpoint of +2 Inches Water.Caused by Instru Drift.Setpoint Reset | | | 05000220/LER-1978-040-03, /03L-0 on 781113: 112 Core Spray Topping Pump Motor Breaker Closed Starting Pump But Breaker Closing Spring Motor Was Running Continuously & Not Charging Closing Spring.Caused by Misaligned Motor Assembly at Latching Pawl | /03L-0 on 781113: 112 Core Spray Topping Pump Motor Breaker Closed Starting Pump But Breaker Closing Spring Motor Was Running Continuously & Not Charging Closing Spring.Caused by Misaligned Motor Assembly at Latching Pawl | | | 05000220/LER-1978-040, Forwards LER 78-040/03L-0 | Forwards LER 78-040/03L-0 | | | 05000220/LER-1978-041, Forwards LER 78-041/04T-0 | Forwards LER 78-041/04T-0 | | | 05000220/LER-1978-041-04, /04T-0 on 781220:during Impingement Sampling Only 23 Samples (22 Hourly Samples & One 2-hr Sample) Were Collected Instead of 24 Required Samples,Caused by one-time Personnel Scheduling Change | /04T-0 on 781220:during Impingement Sampling Only 23 Samples (22 Hourly Samples & One 2-hr Sample) Were Collected Instead of 24 Required Samples,Caused by one-time Personnel Scheduling Change | |
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