ML16342D520

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Insp Repts 50-275/96-23 & 50-323/96-23 on 961110-1221. Violations Noted.Major Areas Inspected:Operations,Maint, Engineering & Plant Support
ML16342D520
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 01/17/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION IV)
To:
Shared Package
ML16342D521 List:
References
50-275-96-23, 50-323-96-23, NUDOCS 9701280375
Download: ML16342D520 (52)


See also: IR 05000275/1996023

Text

ENCLOSURE 2

U.S. NUCLEAR REGULATORY COMMISSION

REGION IV

Docket Nos.:

50-275, 50-323

License Nos.:

DPR-80, DPR-82

Report No.:

50-275/96023, 50-323/96023

Licensee:

Pacific Gas and Electric Company

Facility:

Diablo Canyon Nuclear Power Plant, Units

1 and 2

Location:

Dates:

7 1/2 miles NW of Avila Beach

Avila Beach, California

November 10 through December 21, 1996

Inspectors:

M. Tschiltz, Senior Resident.Inspector

S. Boynton, Resident Inspector

D. Allen, Reactor Inspector

G. Good, Emergency Preparedness

Inspector

D. Corporandy,

Project Inspector

Approved By:

H. Wong, Chief, Branch

E

Division of Reactor Projects

ATTACHMENT:

Supplemental

Information

970i280375 970il7

PDR

  • DOCK 05000275

8

PDR

0

-2-

EXECUTIVE SUMMARY

Diablo Canyon Nuclear Power Plant, Units

1 and 2

NRC'Inspection Report 50-275/96023; 50-323/96023

~Oerations

Control room operators

and fire brigade members responded

appropriately in

accordance

with approved procedures to a reactor trip and electrical fire on

November 22, 1996.

Operators promptly assessed,

identified, and dealt with

equipment anomalies.

Response

in combatting the fire was cautious with

appropriate concern for both personnel

and plant safety (Section 01.2).

Clearance

process weaknesses

were identified in that the authorization list was out

of date, training had not been provided even though recent changes

had been made

to the clearance

procedure,

and the transfer of the work between the shift foreman

and the plant operator was unclear in the clearance

procedure.

In addition,

corrective actions were delayed in response

to a previous action request because

the issue was categorized

as nonquality related and was being given a low priority

(Section 01.3).

The licensee's review of past surveillance test results raised concerns about the

basis for both the reliability and continued operability of the 4kV bus first level

undervoltage

relays (FLURs). Following identification of the concern, the licensee

carefully considered

the potential for common mode failure.

Licensee management

directed that confirmatory testing be conducted

promptly to fully assess

the

operability of the relays.

Investigation of the root cause of the problem led to the

implementation of a change

in the relay settings to improve reliability. Licensee

management's

response

to the issue was prompt and decisive and demonstrated

the appropriate concern for safety and sensitivity of the need for compliance with

Technical Specifications

(TS) (Section M1.1.2).

Maintenance

Mechanical maintenance

personnel identified a deficiency in a check valve being

installed in the auxiliary saltwater (ASW) system.

Identification and correction of

the problem by involved maintenance

and quality assurance

personnel demonstrated

an awareness

of potential problems associated

with the maintenance,

a questioning

attitude and appropriate follow through in resolving concerns

raised during

maintenance

activities (Section M1.1.1).

Since 1993, 4kV FLUR surveillance test results indicated that the relay response

to

degraded

voltage was found to exceed the TS allowed response

time on 8 separate

occasions.

This performance

had been considered

acceptable without performing a

-3-

root cause analysis and determining appropriate corrective actions.

A violation was

identified- (Section M1.1.2).

EnrnineerinE

Failure of maintenance

personnel to remove an information tag referencing

a

temporary gauge upon its removal, and failure of operators to remove the jumper

annotations

from the control room drawings were indicative of both inadequate

work practices and inadequate

control of temporary modifications.

A violation was

identified.

Untimely updating of control room drawings and procedures

requiring

revision

following the installation of a permanent

pressure

gauge demonstrated

a

lack of attention to detail in the implementation of the licensee's

minor modification

design change process

(Section E1.1).

The licensee took prompt action to correct inspector-identified fastener deficiencies

on the vital 480V switchgear.

However, follow-on actions to address the quality

problem were considered

weak in that engineering

failed to recognize the need to

document

in an AR the deficiencies for evaluation and resolution in accordance

with

plant procedures.

A violation was identified (Section E2.1).

The licensee identified past occurrences

where a degraded

230kV offsite power

source would have resulted in the component cooling water system being unable to

mitigate the consequences

of a design basis loss of coolant accident.

A noncited

violation was identified (Section E8.1).

TS required Plant Staff Review Committee (PSRC) reviews of safety evaluations for

core reloads and fuel sipping activities completed under the provisions of

10 CFR 50.59, were not performed.

A violation was identified (Section E8.2).

Plant Su

ort

~

The licensee's

emergency

plan and implementing procedures

did not clearly describe

their onshift dose assessment

capability.

Further evaluation of the information

obtained using the temporary instruction will be conducted

by NRC Headquarters

personnel

(Section P3.1).

Re ort Details

Summer

of Plant Status

Unit 1 began this inspection period at 100 percent power.

On November 22, 1996, the

unit tripped dae to an electrical fault associated

with a grounding transformer for unit

Auxiliary Transformer 1-1.

The unit remained in Mode 3 while repairs were made to the

affected buswork.

Unit 1 reentered

Mode

1 on November 30 and was returned to 100

percent power on December 2. The unit remained at full power for the balance of the

inspection period.

Unit 2 began this inspection period at 100 percent power.

The unit remained at full power

throughout the inspection period.

I. 0 erations

01

Conduct of Operations

01.1

General Comments

71707

Using Inspection Procedure 71707, the inspectors conducted

frequent reviews of

ongoing plant operations.

In general, the conduct of operations was professional

and safety conscious.

01.2

Unit 1 12kV Electrical Fault and Plant Tri

a.

Ins ection Sco

e 71707

On November 22, an electrical fault and fire in a grounding device associated

with

unit Auxiliary Transformer

1-1 resulted in a unit trip and reactor trip. The inspectors

responded

to the control room and observed

operator actions in response

to the trip

and to the electrical fire.

b.

Observations

and Findin s

The operating crew performed well in response

to the event.

The immediate actions

of Procedure

E-O, "Reactor Trip or Safety Injection," and Procedure

E-0.1, "Reactor

Trip Response,"

were taken in a timely manner.

The operators generally

communicated

these actions clearly and concisely.

The inspectors

noted several equipment anomalies that complicated operator

response.

These anomalies, which included loss of the main condenser

and failure

of one of the intermediate range nuclear instruments to properly track reactor

power, were promptly identified and addressed

by the operating crew.

In response

to the loss of the main condenser,

operators

closed the main steam isolation valves

and established

decay heat removal via the atmospheric

steam dumps in

accordance

with Procedure

E-0.1.

The failure of the intermediate range nuclear

instrument to track reactor power prevented

the source range instruments from

automatically reenergizing when power reached their permissive setpoint (P-6).

-2-

Operators manually reenergized

the source range instruments when power fell

below<h8" P-6 Setpoint.

The fire brigade responded

to the location of the electrical fault within 10 minutes

after the control room announced

the fire. The unit trip and the transfer of the

12kV busses to startup power isolated the fault within the first second of the event

and extinguished the electrical fire. Although some Class A material (e.g. cable

insulation) continued to smolder for several minutes, the fire was essentially out

when the fire brigade arrived.

Although no further firefighting efforts were required

at the scene, the shift supervisor directed the evacuation of the Unit 1 turbine

building until a thorough walkdown could be performed to assess

collateral damage

or hazards.

Licensee Event Report (LER) 50-275/96-017,

Revision 0, documented

the automatic reactor trip. The inspectors reviewed the

I ER and determined the specified

corrective actions were appropriate to prevent recurrence.

Based upon this review

the LER is closed.

c.

Conclusions

Licensee personnel

responded

well to the reactor trip and electrical fire on

November 22.

Operators promptly identified and addressed

equipment anomalies.

The operations staff also showed an appropriate sensitivity to personnel safety in

responding to the fire.

01.3

Review of the Diablo Can on Power Plant

DCPP

Clearance

Process

a.

Ins ection Sco

e

In light of past problems with the licensee's clearance

process,

the inspector

reviewed Procedure

OP2.ID1, "DCPP Clearance

Process,"

and guidance

on

"Management Expectations for Supervisors"

issued on February 23, 1996.

The

inspectors

also reviewed the thoroughness

and quality of the licensee's review and

response

to Action Request

(AR) A0396913 which sought clarification on the

February 23 guidance

as it applied to Procedure

OP2.ID1 and which pointed to

potential problems with the guidelines as they applied to Procedure

OP2.ID1.

b.

Observations

and Findin s

The current revision of Procedure

OP2.ID1, Revision 5, consists of a master

clearance/ subclearance

concept.

A master clearance

is used to isolate work

boundaries

and track the status of plant equipment

as work is performed.

Work is

authorized by issuing a subclearance

to a group or department performing work

within the boundary of the master clearance.

0

-3-

In the clearance

process, the shift foreman (SFM) is responsible for reviewing

procedure's

to"Bear and restore cq.:ipment, and the Master Clearance

Holder is

responsible

for overseeing

the proper implementation of the procedures.

Procedure

OP2.ID1 allows for the Master Clearance

Holder to be the SFM or

another person qualified for such tasks.

The inspectors noted that Section 3.4 of

the procedure stated that "...the Master Clearance

Holder should have

documented

training on the clearance procedure

and be on the qualified Clearance

Requestor/Delegate

Authorization list." The inspectors briefly reviewed this list with

a licensee representative,

who noted that the list had not been updated

in years.

Some individuals on the list had long ago left the organization.

It was further noted

that training had not recently been provided to the individuals on the list even

though Procedure

OP2.ID1 had recently undergone

several revisions.

Section 4.4.12 of Procedure

OP2.ID1 requires routing of all Master Clearances to

the SFM for processing.

Section 4.6.1 requires that the senior control operator is

responsible for ensuring the plant operator assigned to process the clearance;

is

properly qualified.

The inspectors noted that Procedure

OP2.ID1 did not clearly

define how the clearance

processing

activities move from the SFM to the plant

operator.

At the time of the inspection, the licensee was in the process of revising

Procedure

OP2.ID1 to clarify the clearance process.

The licensee pointed out that

the draft of the upcoming revision to Procedure

OP2.ID1 contained wording to

require the Master Clearance

Holder to be the SFM.

When issued, Revision 6 of

Procedure

OP2.ID1 will be reviewed to verify that the Master Clearance

Holder is

the SFM and that responsibilities and delegation, where applicable, are clearly

delineated

in the procedure

(IFI 50-275(323)/96023-01).

During the review process,

the inspectors

noted that AR A0396913 was initiated

on March 26, 1996, and on the following day an individual was assigned to respond

to the AR. Procedure

OM7.ID1, "Problem Identification and Resolution - Action

Requests,"

defines

a Quality Problem as "...a deficiency which renders or could

render a quality related item or activity unacceptable

or indeterminate."

Action

request forms contain a "Quality Problem Checklist" section wherein each checklist

item is required to be answered.

The AR is automatically considered

a Quality

Problem, if anything other than a "N" appears

in one of the fields.

AR A0396913

was determined not to be a Quality Problem.

The Quality Assurance

(QA) Class

field was marked as "N" indicating "not subject to QA requirements."

The

inspectors noted that the "N" in the QA Class field was inappropriate

because

Procedure

OP2.ID1, a QA-related procedure,

was one subject of the concerns

in the

AR.

For the period from March 27, 1996, to December

13, 1996, the licensee had not

formally documented

any action taken on AR A0396913.

According to the

licensee, dispositioning of an AR that was not a Quality Problem would not be of

high priority. According to the individual assigned

to the AR, work was being done

4

to address the concerns

raised in the AR, and this was evidenced

by the current

work'to revis'e Procedure

OP2.ID1.

c.

Conclusions

The inspectors considered

the lapses

in training on the DCPP Clearance process,

the

licensee's failure to keep the Requestor/Delegate

authorization list current, and the

ambiguities in the current revision of Procedure

OP2.ID1 to be evidence of a

weakness

in the licensee's

clearance

process.

The inspectors

also considered that

the licensee's

response to problems identified in AR A0396913 lacked formality and

timeliness.

II. Maintenance

M1

Conduct of Maintenance

M1.1

Maintenance

Observations

a.

Ins ection Sco

e 62707

The inspectors observed

all or portions of the following work activities:

C0147525

Replace ASW Vacuum Breaker

C0146910

Replace Centrifugal Charging (CC) Pump 1-1 Gear Drive Lube

Oil Heat Exchanger (Unit 1)

b.

Observations

and Findin s

The inspectors found the work performed under these activities to be accomplished

in accordance

with procedures.

All work observed was performed with the work

package present and in active use.

Technicians were experienced

and

knowledgeable

of their assigned

tasks.

The inspectors observed the system

engineer monitoring job progress during the replacement

and testing of the gear

drive lube oil heat exchanger.

Additional observations

on the ASW vacuum breaker

replacement work are provided in the following section.

M1.1.1

Re lacement of ASW Vacuum Breakers

a.

Ins ection Sco

e 62707

On December 4, the inspectors

observed

portions of the activities associated

with

the replacement of two of the Unit

1 ASW piping vacuum breakers.

-5-

b.

Observations

and Findin

s

The ASW vacuum breakers were being replaced with identical swing check valves

with the exception that the new valves incorporated

a teflon surface to the valve

seat.

The teflon seating surface was installed to alleviate the potential for bonding

of the valve seat to disc mating surface which could occur over long periods of

inactivity of the valve.

The vacuum breakers

are located within a concrete vault outside of the plant

protected area.

The inspectors noted that proper security measures

were taken

while the vault was open and accessible.

Rigging equipment utilized for the vault

cover and the valves was in accordance

with plant procedures.

During installation of the first valve, the mechanical maintenance

personnel

noted

that the valve disc would not swing freely.

The maintenance

personnel

rejected

the valve and took action to obtain another valve from stock.

The system engineer

and mechanical maintenance

foreman responded

to address

corrective actions

following identification of the defective valve.

These actions demonstrated

a strong

questioning attitude.

c.

Conclusions

The replacement

of the ASW vacuum breakers

and the supporting activities were

performed in accordance

with plant procedures.

The identification of the defective

valve by the maintenance

personnel demonstrated

a questioning attitude and

appropriate follow through in resolving concerns

raised during maintenance

activities.

M1.1.2 4kV FLUR Re lacement

Ins ection Sco

e 62707

The inspectors reviewed the surveillance results from testing performed for the past

three outages

on the 4kV FLURs.

During the review the inspectors referenced the

following documents:

AR A0352900 documenting 4 kV undervoltage

relay out of tolerances

AR A0418008 documenting placement of the 4kV system in goal

setting

Surveillance Test Procedure

M-75, Revision 15, "4kV Vital Bus

Undervoltage

Relay Calibration"

Maintenance

Procedure

E-50.10B, Revision 7, "General Electric Type

lAV55C Undervoltage

Relay Maintenance"

0

-6-

~

Design Criteria Memorandum S-63, Revision 1.3,"4160 System,"

Section 4.3.5.2

Nonconformance

Report 2007, 4kV Undervoltage Protection

4

DCPP TS Table 3.3.4, Engineered

Safety Features Actuation System

Instrumentation Trip Setpoints

LER 50-275(323)/96-018

Revision 0: "4kV Bus Undervoltage

Protection Relays Out of Specification Due to Setpoint Drift Due to

Unknown Cause."

b.

Observations

and Findin s

During the licensee's review of 4kV FLUR test results from previous outages,

the

licensee noted that the relays had failed TS required surveillance tests due to their

as-found time delays at 2583 volts exceeding the maximum 10 second interval

specified in TS Table 3.3-4.

Review of the test data revealed that during the

18 relay tests performed during the past 3 Unit

1 and 2 refueling outages,

eight

relays had as-found time delays of greater than the 10 second limit specified in TS.

Assessment

of 4kV FLUR 0 erabilit

After identification of the numerous test failures, the licensee wrote a prompt

operability assessment

(POA). The POA noted that the FLUR has two functions.

The first function is to detect

a low bus voltage at approximately 60 percent of the

nominal bus voltage and allow a maximum of 10 seconds

in order to allow transfer

from a degraded

auxiliary power source to startup power before starting the

Emergency

Diesel Generator

(EDG). The second function is to start the EDG which

supplies the associated

4kV bus within 0.7 seconds

of detecting

a dead bus.

The

operability of the first function of the relay was in question since the eight test

failures were due to exceeding the maximum allowed time delay of 10 seconds.

The delayed start of the EDG is also accomplished

by a separate

design feature, the

second

level undervoltage

relay (at approximately 3800 volts).

In a degraded

voltage condition, the secondary

undervoltage

relay actuation of the delayed start of

the EDG and the 4kV load shed would occur before the FLUR actuation.

Therefore,

the FLUR out of tolerance time delay would not have prevented the performance of

this safety function.

Mana ement

Res

onse to Historical Surveillance Test Results and the POA

Plant management's

review of the POA determined that the FLUR relays should be

considered

operable until testing was accomplished.

However, management

directed that the testing be performed as soon as possible since past data provided

strong evidence that some of the relays could be expected

be out of specification

0

-7-

during the operating cycle.

While making preparations for the relay testing it was

determined that there was only one spare relay of this type onsite.

The licensee

calibrated the spare relay on the bench and then removed

EDG 1-3 from service,

replaced its FLUR with the spare,

and tested the previously installed relay. Test

results indicated that the relay was set within the TS requirements.

Prior to

continuing, the licensee implemented

a design change to adjust the relay settings so

that the time delay feature would be less subject to change.

The licensee continued

with the one for one exchange

and testing of the relays until the FLURs for all six

EDGs were replaced with relays calibrated with the new settings.

Of the six relays

tested, one was found to be outside the TS specified time with an as-found time

delay of 11.8 seconds.

The licensee has initiated a nonconformance

report on this

problem.

Past Corrective Actions for 4kV FLUR Test Failures

Review of the ARs which documented

the previous surveillance test failures

revealed that in October 1994 the licensee noted that the FLURs had exhibited what

was characterized

as excessive drift for which there was no conclusive cause.

At

that point, the licensee planned on monitoring future performance of the relay in

order to determine if broader corrective action was warranted.

AR A0352900

noted that a quality evaluation would not be issued until additional test results were

obtained which would allow for further trending of relay performance.

The licensee's justification for not issuing a QE noted that the relay functioned

properly for a dead bus condition and that the increase

in the time delay above that

allowed by TS did not impact safety.

The AR also had an action to track the future

relay performance

and evaluate whether broader corrective actions were warranted.

Although additional relay surveillance test failures occurred and were documented

in

the AR, no additional actions were taken for determining the root cause of the

failures until November 1996.

The failure of the licensee to assure that the cause

of the excessive

relay drift was determined

and take corrective action to preclude

recurrence

is a violation of 10 CFR Part 50 Appendix B Criterion XVI

(VIO 50-275 (3231/96023-02).

Conclusions

Management

responded

appropriately once concerns were raised regarding past

relay surveillance test results.

However, based

upon the number of tests with

out-of-specification results, the existing surveillance program did not provide

adequate

assurance

that the relay was capable of performing its required function

during an entire 18 month operating cycle.

In addition, corrective actions taken

following repeated

out-of-specification relay test results failed to identify and correct

the cause of the exceeding

TS specified limits.

-8-

M1.2

Surveillance Observations

a.

Ins ection Sco

e 61726

The inspectors observed

all or portions of the following surveillances:

STP R-2B2, Revision 5, "Manual Operator Heat Balance"

~

STP P-AFW-11, Revision 4, "Routine Surveillance Test of Turbine-Driven

Auxiliary Feedwater

Pump 1-1"

b.

Observations

and Findin

s

The inspectors found that the surveillance tests reviewed and/or observed were

being scheduled

and performed at the required frequency.

The procedures

governing the surveillance tests were technically adequate

and personnel performing

the surveillance demonstrated

an adequate

level of knowledge.

The inspectors

also

noted that test results were appropriately dispositioned.

M8

Miscellaneous Maintenance Issues (92902)

M8.1

Closed

IFI 50-275 96021-05:

During a review of the completed work order (WO)

that replaced the motor for residual heat removal (RHR) Pump 1-1, adequate

documentation

could not be found to demonstrate

that the motor had been properly

assembled

to the pump in accordance

with the new motor's seismic qualification

evaluation

(SQE) (PGRE Calculation SQE-46) using the required bolt torque of

124 ft-lbs.

The licensee also reviewed the calibration sheets for the maintenance

and test

equipment (MRTE) utilized during change out of the RHR 1-1 motor.

The licensee

found that maintenance

personnel

had requested

the calibration lab to verify a

torque value of 124 ft-Ibs for the torque wrench utilized in the pump/motor

reassembly activity. Since no other specified torque value was called out for the

MRTE used in that activity, the licensee concluded that hold down bolts had been

properly torqued.

The licensee has initiated several corrective actions in response

to the

inspectors'oncerns

regarding the WO documentation

and is tracking those actions through

AR A0417470.

The licensee will be:

(1) revising Procedure

MP M-10.1 to add line

items for the installation of the motor hold-down bolts, (2) reviewing

Procedures

MP M-10.1 and E-10.1 to assure that component nomenclature

is

-9-

consistent between them, and (3) adding the specified torque of 124 ft-Ibs to the

RHR.pump drawing.

Conclusions

WO C0116037 and Procedures

MP M-10.1 and E-10.1 were unclear in that they

failed to provide a link to the implementation of the requirements

specified in PGSE

Calculation SQE-46.

The inspectors considered

this to be a weakness

in the

documentation

of safety-related

maintenance

to assure continued seismic

qualification.

E1

Conduct of Engineering

E1.1

Reactor Coolant Letdown Filter Desi

n Chan

e

a.

Ins ection Sco

e

37551

The inspectors reviewed the licensee's activities associated

with the installation of

permanent

pressure

gauges downstream of the No. 2 reactor coolant letdown filters

for Units

1 and 2. The review included the licensee's evaluation and conclusions

on

the impact of the design change on plant drawings, procedures

and maintenance.

b.

Observations

and Findin s

Due to a historical design deficiency, direct measurement

of the differential pressure

across the No. 2 letdown filter could not be made when the No.

1 filter was

isolated.

Specifically, the common downstream

pressure

gauge for both filters was

located within the isolation boundary for the No.

1 filter. To provide for direct

measurement

of the differential pressure

across the No. 2 filter the licensee installed

a temporary pressure

gauge (PX-342) downstream of the No. 2 filter. This

temporary modification (jumper) was controlled under Procedure

CF4.ID7,

Revision 3, "Temporary Modifications - Plant Jumpers

and

M5TE." The design

change, documented

under maintenance

modification (AT-MM)AR A0367186 for

Unit

1 and A0367188 for Unit 2, was implemented to eliminate the need for the

temporary jumper.

The new pressure

gauges

(Pl-2505) were physically installed in

the units in October 1996.

Tem orar

Jum

er Controls

On November 4, 1996, the inspectors noted during a plant tour that the physical

installation of both permanent

pressure

gauges

was complete and that the

temporary gauges

had been removed; however, an information tag remained on the

root valve to the new pressure

gauge on Unit 2 indicating that temporary

Gauge PX-342 was still installed.

The Unit 2 control room operating valve

-10-

identification diagram (OVID) ¹ 107708, Sheet 4, also contained annotations

showing the. installation of the temporary gauge.

The Unit 2 jumper log, however,

documented

the removal of the temporary gauge on October 30.

The

documentation

available to the operators

did not reflect current plant configuration.

Procedure

CF4.ID7 requires all information tags and drawing annotation sheets to

be removed when a temporary modification is removed.

The failure of maintenance

personnel to remove the temporary jumper information tag on Unit 2 and the failure

of operations

personnel to remove the drawing annotations

indicate a failure in the

licensee's

configuration controls for temporary modifications and is a violation of

Procedure

CF4. ID7 (VIO 50-323/96023-03).

Plant Drawin s

On December 2, the inspectors attempted to verify that the control room copies of

the plant drawings affected by the design change

had been updated.

However, it

was identified that two of the three piping and instrument drawings (PKIDs)

affected on Unit

1 and all three of the PSIDs affected on Unit 2 contained only

temporary sketches of the modification without indication that the modification had

been completed.

Additionally, the affected Unit 2 chemical and volume control

system (CVCS) OVID did not reference the new gauge.

The licensees

processes

for updating plant drawings are described,

in part, in

Procedure

CF3.ID6, Revision 2, "Field Correction Transmittal (FCT) Processing,"

and

Procedure

OP1.DC21, Revision 1A, "Development and Control of Plant Operating

Valve Identification Diagrams and Instrument Prints."

Step 5.10.1 of

Procedure

CF3,ID6 states that Priority

1 drawings, such as PSIDs, should be

updated within 30 days of engineering

acceptance

of the FCT. AT-MM

AR A0367186 documented

engineering's

acceptance

of the Unit

1 FCT on October

24 while AT-MMAR A0367188 documented

engineering's

acceptance

of the Unit

2 FCT on November

1. The time delay between the acceptance

of the FCTs and

the update of the PSIDs in the control room did not meet the expectations

of

Procedure

CF3. ID6.

In accordance

with Procedure

OP1.DC21, OVID revisions are requested

via a OVID

change transmittal (OCT). The OCT, submitted by the sponsoring

engineer of a

design change,

is processed

by the OVID office supervisor and then forwarded to

Document Services for distribution to controlled copy holders.

An OCT is closed

out when the OVID office supervisor issues the revised OVID incorporating the

changes

of the OCT. The OCTs for this design change were completed by the

sponsoring

engineer and forwarded to the OVID office supervisor who processed

them on November 1.

On December

2, the inspectors found that the control room

copy of the Unit 2 CVCS OVID did not yet reflect the design change.

-1 1-

0 eratin

Procedures

and Lo s

As part of the design change process,

operations evaluated the impact of the new

pressure

gauges

on operating procedures.

The evaluation concluded that

Attachments 9.3 and 9.4 of Procedure

OP B-1A:IX, "CVCS - Valve Alignment

Verification Checklist for Plant Startup," required revision to reflect the new gauge

and its associated

valves.

An on-the-spot-change

(OTSC) to Procedure

OP B-1A:IX

was issued on November 20 to reflect those revisions.

However, Attachment 9.2

was also impacted by the design change,

but had not been revised.

Attachment 9.2 contained

a note to ensure that the downstream

isolation valve for

the No.

1 filter is open so that differential pressure

across the No. 2 filter can be

determined.

The design change eliminated the need for this action.

The operating logs utilized by the auxiliary operators were also identified by the

inspectors

as being impacted by the design change.

The daily rounds sheets

and

their associated

technical bases provide for documentation

and evaluation of various

plant process parameters,

including the differential pressure

across the letdown

filters. These documents

had not been updated to reflect the availability of the

permanent

gauge.

Conclusions

The failure of maintenance

personnel to remove the information tag referencing

temporary Gauge PX-342 upon its removal, and the failure of operators to remove

the jumper annotations from the Unit 2 OVIDs indicated

a lack of attention to detail

by operations

in the implementation the licensee's temporary modification program.

The delays in updating plant drawings associated

with the installation of permanent

Gauge Pl-2505 and the failure to promptly identify and update all of the affected

procedures

and documents

used by operations demonstrated

a lack of rigor by

operations

in the minor modification design change process.

Reactor Coolant S stem

RCS

Flowrate Determination Test Chan

es

Ins ection Sco

e 37551

The inspectors reviewed the actions taken by the licensee when the change was

made to perform the measurement

of RCS flow at the end of cycle.

In addition, the

inspectors reviewed a TS interpretation for the setting of the RCS loss of flow

protection trip setpoints.

Observations

and findin s

The licensee measures

RCS flow by performing a heat balance (calorimetric) on

each side of the steam generator.

To avoid the potential for future derating of the

units due to reductions in the calculated

RCS flowrate due to the bias effect of hot

-1 2-

leg temperature

streaming, the licensee performed

a flow uncertainty analysis to

evaluate the possibility of changing the performance of primary flow calorimetrics

from the beginning of cycle (BOC) to the end of cycle (EOC).

Historically, the licensee has performed

a primary flow calorimetric at the BOC

during initial power ascension.

Based upon the results of the uncertainty analysis,

the licensee concluded that it was acceptable to perform primary flow calorimetrics

using EOC data.

Following 1R6 and 2R6 the licensee made the change to perform

primary flow calorimetrics at the EOC.

The licensee did not perform a safety

evaluation prior to making the change

and the PSRC was not required to review

since the technical review determined that the change

did not alter the intent of the

procedure.

Hot Le

Tem erature Streamin

Effects

Although the uncertainty associated

with performing the analysis at EOC was

greater than the uncertainty at BOC, the actual calculated flowrate was higher due

to the effect of the higher than actual measured

hot leg temperatures

at the BOC

caused

by hot leg temperature

streaming.

The hot leg temperature

streaming effect

is more pronounced

at the BOC than at the EOC due to the relative decrease

in the

difference in the power output of the inner and outer regions of the core during the

cycle.

Hot leg temperature

streaming occurs as a result of the combined affect of low

leakage core designs, that have a higher percentage

of core power produced

in the

inner core regions, and incomplete mixing of flow in the upper plenum.

Low

leakage core loading was first used in by the licensee

in 1R3.

However, up to 1R6

and 2R6 the hot leg temperature was measured

by resistance temperature

detectors

(RTDs) installed in the bypass lines.

This allowed for greater mixing of flow prior to

the measurement

of hot leg temperature.

Thus, the impact of low leakage cores

was offset by the greater mixing prior to 1R6 and 2R6.

Effect of RTD Thermowell Installation on Measured Tem erature

During 1R6 and 2R6 the licensee removed the RTD bypass lines and installed RTD

thermowells in both hot and cold legs at 120 degree intervals around the

circumference of the pipe.

These design changes

were performed in conjunction

with the installation of the Eagle 21 microprocessor-based

process protection

system.

Following the installation of the thermowells, the RTDs sensed

an

increased temperature

distribution across the cross section of the pipe.

The effect

of hot leg temperature

streaming is more prominent at Diablo Canyon,

as compared

to other Westinghouse

design facilities that utilize low leakage core loading,

because

the hot leg RTDs are installed closer to the reactor vessel due to physical

constraints.

-13-

The hot leg temperature

measurement

is biased by the temperature

streaming which

causes the measured

temperature to be greater than the actual temperature.

This

results in the measured

RCS flowrate being lower than the actual flowrate.

The net

effect of the hot leg temperature

streaming error was a reduction in the margin to

the TS minimum measured flow. Since hot leg streaming is less pronounced

at the

EOC the bias is less and the measured

RCS flowrate increases

so that there is less

difference between measured

and actual flowrates.

However, the performance of

the primary flow calorimetric at the EOC involves additional uncertainties that must

be accounted

for in the analysis which are not included as a part of the BOC

uncertainty.

RCS Flowrate Measurement

Uncertaint

The accuracy of performing RCS flowrate determination at the BOC using

a primary

flow calorimetric is based upon

a detailed flow uncertainty analysis for plant-specific

instrumentation.

A flowrate uncertainty of 2.4 percent of thermal design flow (TDF)

for Units

1 and 2 is noted in TS Figures 3.2-3a and 3.2-3b.

The licensee calculated

the total uncertainty or excess random error associated

with measuring

RCS

flowrate at the EOC was approximately 2.9 percent of TDF. Since the uncertainty

was approximately 0.5 percent greater than the 2.4 percent of TDF included in TS,

the licensee applied a flow penalty of 0.5 percent.

The licensee's

procedure for performing the primary flow determination was revised

to include the use of flow penalties to ensure that minimum measured flow and

safety.setpoint

analysis limit requirements

were met.

The licensee considered the

treatment of the excess flow measurement

uncertainty as a flow penalty to be

conservative.

RCS Low Flow Tri

Set pints

The primary flow calorimetric procedure

is also performed by the licensee to provide

a basis for calibrating the pressure

sensors

on the elbow taps for establishing the

setting of the RCS loss of flow (LOF) setpoints

in Table 2.2-1 of the TS.

STP R-26,

"RCS Primary Coolant Flow Measurements,"

specifies the LOF setpoints

be set at

90 percent of the actual loop flowrate, as measured

by the primary flow

calorimetric, but not less than the TS minimum setpoint of 90 percent of minimum

measured

flow. Therefore, the increased uncertainty or error in flow measurement

also affects the flow error contribution to the RCS LOF setpoint specified in TS

Table 2.2-1.

The licensee instituted a flow penalty methodology for accounting for

the uncertainty in excess of 2.4 percent to ensure that the reactor trip on LOF

occurs at or above the safety analysis limit. These uncertainty calculations were

updated following the installation of the ultrasonic feedwater flow measuring device

to reflect additional uncertainties

based upon vendor specifications on equipment

performance.

The calculation results were incorporated into STP R-26.

-14-

Based on the calculated uncertainties,

the TS minimum setpoint was increased to

90.5~rcent of the minimum measured'flow

on Unit 2 to ensure that TS

requirements

continued to be met.

TS interpretation 96-10 was approved by the

PSRC to establish the LOF setpoint at greater than or equal to 90.5 percent.

Although this was greater than the TS specified limit, the licensee considered it

acceptable

since the limit was more conservative than that specified by TS.

NRC Concerns

Re ardin

the Potential For Unreviewed Safet

Questions

Based upon inspector reviews of the licensee's justification for increasing the RCS

LOF trip setpoint above that specified in TS and the licensee's own internal

concerns regarding the acceptability of having a measured flow uncertainty greater

than the 2.4 percent referenced

in TS, a conference

call was conducted to discuss

the issues.

Participants in the call included licensee personnel, the senior resident

inspector,

NRR project manager,

and technical personnel from NRR.

During the

conference

call questions

were raised which indicated that the change

in measuring

RCS flow at the BOC to EOC potentially involved an unreviewed safety question or

involved a change to TS.

Following the conference

call the licensee decided to reset the instrumentation

by

performing primary calorimetric flow determinations,

for both units, based upon data

taken at the BOC. The Eagle 21 scaling constants

and the plant process computer

and vertical board RCS flow constants

were revised based upon BOC RCS flow

calorimetric results for both units.

Following completion of the calculations, the

PSRC TS interpretation that required adjustment of the LOF trip to 90.5 percent was

rescinded.

C.

Conclusions

The licensee's

change to measuring

RCS flowrate at the EOC that was performed

without a formal safety evaluation is being considered

as an unresolved

item

pending further NRC review of the issue (URI 50-275(323)/96023-04).

E2

Engineering Support of Facilities and Equipment

E2.1

480V Vital Switch ear Fasteners

Ins ection Sco

e 71707

37551

On November 19, during a routine tour of the Unit 2 480V vital switchgear rooms,

the inspectors identified a number of loose fasteners

associated

with the breaker

front panels.

These findings were discussed with the system

ngineer and the

onsite mechanical engineer responsible

for seismic qualification and evaluation of

plant equipment.

The inspectors

also reviewed Procedure AD4.ID8, Revision 1,

"Identification and Resolution of Loose, Missing or Damaged

Fasteners."

-1 5-

b.

Observations

and Findin s

The inspectors identified six breaker cubicles on vital Bus 2F, eight breaker cubicles

on vital Bus 2G, and ten breaker cubicles on vital Bus 2H, each with one loose front

panel fastener.

The system engineer took immediate action to verify the

inspectors'bservations

and tighten all of the fasteners.

The system engineer also performed

a

walkdown of the Unit 1 480V vital switchgear and identified a missing fastener on

one of the breaker cubicles for vital Bus 1G.

The system engineer initiated an

AR (A0417578) to replace the missing fastener on Unit 1. An AR was not initiated

to address the loose fasteners

on Unit 2.

On November 22, the system engineer stated that the licensee's

SQE for the 480V

vital switchgear (SQE-42) did address the front panel fasteners.

Specifically, a note

was included in SQE-42 which stated that one missing fastener on each of the

breaker cubicle front panels was acceptable.

This resolved the inspectors'oncerns

regarding the impact of the loose fasteners

on the seismic qualification of the

switchgear; however, it did not address the identified quality problem.

On December 2, the inspector questioned

the system engineer on the need to

initiate an AR to be able to trend the quality problem with the loose fasteners

on

Unit 2. A review of Procedure AD4.ID8 found that an AR is required to be initiated

when loose, missing, or damaged

fasteners

are identified on safety-related

equipment.

The system engineer initiated an AR (A0418696) documenting this

issue on December 3. The failure of the licensee to initiate an AR to address the

loose fasteners

in Unit 2 until prompted by the inspectors

is a violation of Procedure

AD4.ID8 (VIO 50-323/96023-05).

Conclusions

The licensee took prompt action to correct the identified deficiencies.

However,

follow-on actions to address

the quality problem were considered

weak in that

engineering

failed to recognize the need to document the identified deficiencies for

evaluation and resolution in accordance

with plant procedures.

E8

Miscellaneous Engineering Issues (92700, 92903)

E8.1

Closed

LER 50-275 323 95-07

Revisions 0 and 1: 230kV system may not be

able to meet its design requirements for all conditions due to personnel

error.

The

licensee identified 230kV system design vulnerabilities when assessing

the impact

of routine transmission

line maintenance

on 230kV system operability in June 1995.

Subsequent

licensee investigation of the problem identified 47 separate

occasions

during system maintenance,

between 1990 and 1995, when the voltage on the

230kV offsite power system was degraded

such that during a loss of coolant

accident (LOCA), engineered

safety feature (ESF) loads may have first started on

startup power and may have then shifted to the EDGs.

Of the 47 separate

occasions,

19 were less than 30 minutes duration and 26 were of a duration

-16-

between

2 hours2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> and 72 hours8.333333e-4 days <br />0.02 hours <br />1.190476e-4 weeks <br />2.7396e-5 months <br />, with 3 occasions with durations of greater than

7249urs~

Double Se

uencin

Followin

Transfer From a De raded Bus

The starting, stopping, and restarting of ESF loads is referred to as "double

sequencing."

That is, the loads would first be supplied by 230kV startup power,

and subsequently,

following the slow transfer of 12kV loads to a degraded

source

of 230kV power, the EDGs would start due to the actuation of the second level 4kV

bus undervoltage

relays.

In turn, this would cause the ESF loads to shed from the

startup bus and resequence

back on to their respective 4kV busses after the busses

had transferred

and were being powered by the EDGs.

The consequence

of this condition is that component cooling water (CCW) flow to

the containment fan cooler units (CFCU) would be interrupted during the initial

stages of the LOCA. In containment,

the steam would continue to flow across the

CFCU cooling coils and transfer heat to the CCW system during the time the CCW

pumps were deenergized.

The continued heat transfer across the CFCU cooling

coils in combination with the delay of the restart of the CCW pumps would cause

the CCW in the CFCU coils to flash to steam.

Following the restart of the CCW

pump the steam void would collapse and cause

a substantial water hammer.

CCW

system pressure

would rapidly increase

as a consequence

of the collapse of the

steam void, after the restart of the CCW pump.

Conse

uences

of De raded 230kV Offsite Power Source

After performing an in depth evaluation of the consequences

of the degraded

voltage condition, the licensee determined that the peak CCW system pressure

following the collapse of the steam voids would have exceeded

the ultimate

strength of the CFCU cooling coils and result in failure of the system pressure

boundary.

Following failure of CCW system pressure

boundary the CCW system

would not have been able to perform its design safety function. The licensee noted

that although they were unable to demonstrate

with absolute certainty that the

CCW and CFCU systems would have remained operable when the 230kV system

was degraded,

that they continue to have

a reasonable

expectation that further

resource

intensive efforts could possibly reach the conclusion to the contrary.

Rather than continuing to pursue further evaluation,

PG&E has chosen to declare

that these systems were inoperable.

TS 3.7.3.1 requires that at least two vital CCW loops shall be operable

in Modes 1,

2, 3, and 4.

Contrary to this requirement,

during the time periods when the 230kV

system voltage was degraded,

both loops of the CCW system would not have been

able to perform their intended safety function if a design basis LOCA were to have

occurred.

-1 7-

Miti atin

Factors for Enforcement

The inability of a safety system designed to prevent or mitigate a serious safety

event under certain conditions is a violation that is normally considered

for

escalated

enforcement action.

However, in evaluating this particular situation there

are several factors that require consideration.

The degraded

230kV voltage

condition is a design issue that was in existence for more than 3 years and is not

linked to current licensee performance.

The issue involving the degraded

230kV

offsite power source was licensee identified as a result of the licensee's own

voluntary initiative. The potential for degraded

voltage on the 230kV system has

been reduced by procedural controls in the short term and will be further reduced

in

the long term by the installation of variable tap transformers scheduled

during each

unit's next refueling outage.

The vulnerability for flashing of CCW in the CFCUs

has been eliminated by a design change.

The vulnerability of the CCW system

during time periods of degraded

230kV system voltage would not have been

identified by routine efforts, such as surveillance or QA activities.

Consistent with

the guidance

in Section VII.B.3 of NUREG-1600, "General Statement of Policy and

Procedures

for NRC Enforcement Actions," enforcement discretion will be exercised

and the violation will not be cited (NCV 50-275(323)/96023-06).

E8.2

Closed

LER 50-275 323

96-015

Revision 0: TS 6.5.2.6 not met when cores

reloaded without PSRC review of safety evaluations

due to programmatic

deficiency.

During review of the licensee's Monthly Operating Report, the

inspectors questioned

the date listed for the PSRC review and approval of the

Unit 1.Cycle 8 core reload fuel design and core configuration.

The date listed in the

report was after the date for restart after completion of the refueling outage.

Upon

investigation of the issue, the licensee determined that the PSRC had not reviewed

the safety evaluation performed for Unit 1 Cycle 8 core reload. The core reload

'afety evaluations

are performed for the licensee by Westinghouse.

Further investigation by the licensee determined that the Unit 2 Cycle 8 and Unit

1

Cycle 7 reload safety evaluations

also had n'ot been reviewed by the PSRC.

Following discovery, the PSRC performed reviews of the Units

1 and 2 Cycle 8

safety evaluations

and determined that no unreviewed safety questions existed.

Prior to the Unit 2 sixth refueling outage (2R6) the licensee's practice was to attach

the core reload safety evaluations to design change packages

which required PSRC

review.

Following 2R6, the licensee revised their procedures

to include the safety

evaluations

as a part of a maintenance

modification package.

The licensee's

administrative procedures

governing maintenance

modification procedures

do not

require that they be reviewed by the PSRC.

The licensee has initiated a

nonconformance

report on this problem.

It should be noted that the PSRC did review the core operating limits reports for

Unit 2 Cycles 7 and 8 and Unit

1 Cycle 8 as required by TS 6.9.1.8.

The core

operating limits report is generated

by Westinghouse

and submitted to the licensee

as an attachment to the core reload safety evaluation.

The report documents

the

0

-1 8-

required core operating limits necessary

to ensure

all applicable limits of the safety

anaiy-sis are met."

During separate

and subsequent

review of the safety evaluation for fuel sipping

performed during the Unit 2 seventh refueling outage (2R7), the inspector

questioned

whether the safety evaluation had been reviewed by the PSRC and was

informed by the licensee that it had not.

The safety evaluation for fuel sipping

performed for the licensee by Westinghouse

concluded that there were no

unreviewed safety questions associated.

The PSRC review of the fuel sipping

safety evaluation has been scheduled

by the licensee.

The licensee also identified

that the PSRC failed to review safety evaluations for the UFSAR changes that were

incorporated into Revision 11 of the UFSAR.

TS 6.5.2.6 requires that the PSRC shall be responsible for the review of safety

evaluations for:

(a) changes to procedures

and (b) tests and experiments completed

under the provisions of 10 CFR 50.59, to verify that such actions do not constitute

an unreviewed safety question.

The failure of the PSRC to review safety

evaluations for the Unit

1 Cycles 7 and 8 and Unit 2 Cycle 8 safety evaluations

and

the 2R7 fuel sipping safety evaluation is a violation (VIO 50-275(323)/96023-07).

The corrective actions will be reviewed as a part of the review of the licensee's

response to the violation, therefore, the associated

LER 50-275(323)/96-015

Revision 0 is closed.

Conclusion

The licensee's

administrative controls that incorporate the administrative

requirements of TS 6.5.2.6 were ineffective in ensuring these requirements

were

met.

As a result, required PSRC review of safety evaluations performed under the

provisions of 10 CFR 50.59 were not always performed.

E8.3

Closed

LER 50-275 94006-01:

Centrifugal Charging (CC) pump outside of design

basis due to throttling of CCW to subcomponents.

This event was discussed

in

NRC Inspection Report 50-275/96-20; 50-323/96-20.

The inspection report noted

that, although the CCW flow to CC pump heat exchangers

was sufficient, the flow

was less than that recommended

by the vendor.

During the inspection period, the

inspectors observed the replacement

of the gearbox oil heat exchanger

on

CC Pump 1-1.

Due to a more efficient design, the replacement

heat exchanger was

able to provide the required gearbox oil cooling with approximately

10 gpm CCW

flow to the heat exchanger

versus the 32 gpm CCW flow required for the original

heat exchanger.

Post modification testing by the licensee verified that CCW flow to

each of the CC Pump 1-1 heat exchangers

was restored to the design basis cooling

requirements.

The licensee planned to implement the modification on the other

Unit

1 CC pump, as well as the Unit 2 CC pumps within a few weeks.

-19-

IV. Plant Support

P3

Emergency Preparedness

Procedures

and Documentation

P3.1

Licensee Onshift Dose Assessment

Ca abilities

Ins ection Sco

e

Tl 2515 134

Using Temporary Instruction 2515/134, the inspectors gathered information

regarding:

~

Dose assessment

commitments

in the emergency

plan

Onshift dose assessment

emergency

plan implementing procedure

~

Onshift dose assessment

training.

The DCPP Emergency

Plan Revision 3 and the following Einergency Plan

implementing procedures

were reviewed:

EP G-2, Revision 19, "Activation and Operation of the Interim Site

Emergency Organization (Control Room)"

EP R-2, Revision 19A, "Release of Airborne Radioactive Materials Initial

Assessment."

b.

Observations

and Findin s

On December 16, 1996, the inspectors conducted

an in-office review of the

emergency

plan and implementing procedures to obtain the information requested

by the temporary instruction.

The inspectors conducted

a telephone interview with

the licensee on December 18, 1996, to verify the results of the review.

Based on

the documentation

review and licensee interview, the inspectors determined that

the licensee had the capability to perform onshift dose assessments

using real-time

effluent monitor and meteorological data; however, their capability was not clearly

described

in the emergency

plan and implementing procedures.

C.

Conclusion

Although the onshift dose assessment

capability existed, the capability was not

clearly described

in the emergency

plan and implementing procedures.

Further

evaluation of the information obtained using the temporary instruction will be

conducted

by NRC Headquarters

personnel.

-20-

V. Mana ement Meetin s

X1

Exit Meeting Summary

The inspectors presented

the inspection results to members of licensee management

at the

conclusion of the inspection on December 20, 1996.

The licensee acknowledged

the

findings presented.

The inspectors

asked the licensee whether any materials examined during the inspection

should be considered

proprietary.

No proprietary information was identified.

ATTACHMENT

SUPPLEMENTAL INFORMATION

Licensee

J. R. Becker, Director, Operations

T. A. Bennett, Director, Outage Services

K. H. Bych, Director, Nuclear Quality Services

S. G. Chestnut,

Senior Engineer, Nuclear Steam Supply Systems Engineering

T. F. Fetterman,

Director, Instrumentation

and Control Engineering

R.

Gray, Director, Radiation Protection

C. R. Groff, Director, Engineering Services

C. D. Harbor, Senior Engineer, Regulatory Services

B. C. Hinds, Shift Supervisor, Operations Services

S. C. Ketelsen, Supervisor,

Nuclear Quality Services

D. B. Miklush, Manager, Engineering Services

M. N. Norem, Director, Mechanical Maintenance

D. H. Oatley, Manager, Maintenance

Services

J. L. Portney, Supervisor,

Engineering Services

R. P. Powers, Manager, Vice President

DCCP and Plant Manager

0

-2-

INSPECTION PROCEDURES USED

IP 37551: Onsite Engineering

IP 61726: Surveillance Observations

IP 62707: Maintenance

Observations

IP 71707: Plant Operations

IP 71750: Plant Support

IP 92700: Onsite LER Review

IP 92902: Followup - Maintenance

IP 92903: Followup - Engineering

TI 2515/134: Licensee Onshift Dose Assessment

Capabilities

ITEMS OPENED, CLOSED, AND DISCUSSED

~Oened

50-275(323)/96023-01

50-275(323)/96023-02

50-323/96023-03

50-275 (323)/96023-04

50-323/96023-05

50-275(323)/96023-06

50-275(323)/96023-07

IFI

review of revised DCPP clearance

process

VIO

failure to meet maintenance

rule requirements for 4kV

FLURs

VIO

failure to follow procedures

for temporary plant

modifications

URI

change of RCS flow determination from BOC to EOC

without formal safety evaluation

VIO

failure to document switchboard fastener quality

problem on an action request as required by procedure

NCV

degraded

source of 230kV offsite power

VIO

PSRC did not review safety evaluations

as required by

TS

Closed

50-275(323)/96-01 5-00

LER

50-275/96-01 7-00

LER

50-275(323)/96-018-00

LER

50-275/96021-05

50-275/94006-01

IFI

LER

50-275(323)/96023-05

NCV

50-275(323)/95-07-00,01

LER

degraded

source of 230kV offsite power

230kV system may not be able to meet its design

requirements for all conditions due to personnel

error

TS 6.5.2.6 not met when cores reloaded without PSRC

review of safety evaluations

due to programmatic

deficiency

Automatic reactor trip due to 12kV fault

4kV bus undervoltage

protection relays out of

specification due to setpoint drift due to unknown

cause

RHR pump 1-1 motor hold down bolts torque

documentation

CC pump outside of design basis due to throttling of

CCW to subcomponents

~

~

I

0

-3-

LIST OF ACRONYMS USED

AR

ASTM

ASW

BOC

CC

CCW

CFCU

CVCS

DCPP

EDG

EOC

ESF

FCT

FLUR

LER

LOCA

LOF

MPFF

M5TE

OCT

OTSC

OVID

PDR

POA

PSRC

PAID

RCS

RHR

RTD

SFM

SQE

TDF

TS

UFSAR

WO

action request

American Society for Testing and Materials

auxiliary saltwater

beginning of cycle

centrifugal charging

component cooling water

containment fan cooler unit

chemical and volume control system

Diablo Canyon Power Plant

emergency

diesel generator

end of cycle

engineered

safety feature

field correction transmittal

first level undervoltage

relay

licensee event report

loss of coolant accident

loss of flow

maintenance

preventable functional failure

maintenance

and test equipment

OVID change transmittal

on the spot change

operating valve identification diagram

public document room

prompt operability assessment

plant staff review committee

piping and instrumentation

diagram

reactor coolant system

residual heat removal

resistance temperature detector

shift foreman

seismic qualification evaluation

thermal design flow

Technical Specification

Updated Final Safety Analysis Report

work order