ML16341G635

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Insp Repts 50-275/92-16 & 50-323/92-16 on 920421-0601. Violations Noted.Major Areas Inspected:Plant Operations, Maint & Surveillance Activities & Followup of Onsite Events
ML16341G635
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 07/07/1992
From: Johnson P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML16341G634 List:
References
50-275-92-16, 50-323-92-16, NUDOCS 9207270296
Download: ML16341G635 (48)


See also: IR 05000275/1992016

Text

U.S.

NUCLEAR REGULATORY COMMISSION

REGION V

Report Nos:

Docket Nos:

License

Nos:

Licensee:

Facility Name:

Inspection at:

50-275/92-16

and 50-323/92-16

50-275

and 50-323

DPR-80 and DN-82

Pacific

Gas

and Electric Company

77 Beale Street,

Room 1451

San Francisco,

California 94106

Diablo Canyon Units

1 and

2

Diablo Canyon Site,

San Luis Obispo County,

California

Inspection

Conducted:

April 21 through June

1,

1992

Inspectors:

P. Morrill, Senior Resident

Inspector

M. Miller, Resident

Inspector

Approved by:

Summary:

P.

H.

ohnson,

Chief

Reac

r Projects

Section

1

~(~(~~

Date Signed

Ins ection

on

A ril 21 throu

h June

1

1992

Re ort Nos.

50-2

5 92-16

and

50-323 92-16

1

t d:

t tt

t

p tt

1 pt

t

p

tt

,

1 t

d

surveillance activities, followup of onsite events,

open items,

and licensee

event reports

(LERs),

as well as selected

independent

inspection activities.

Inspection

Procedures

37051,

50073,

61726,

62703,

71707,

71710,

92700,

92703,

93702,

and 94600 were used

as guidance during this inspection.

Safet

Issues

Mana ement

S stem

SINS

Items:

None

Results

General

Conclusions

on Stren ths

and Weaknesses

Strengths:

A more conservative

approach to the scheduling of Instrumentation

and

Control surveillances

was noted.

This involved

a licensee initiative to

discontinue routine use of the

25X grace period allowed by the Technical

Specifications for the performance of surveillances

(paragraph 6.a).

9207270296

920707

PDR

ADOCK 05000275

8

PDR

i

Meaknesses:

The

NRC identified several

problems which had not been identified or

appropriately

documented

by the licensee.

These included the installa-

tion of plastic tarps in front of Appendix

R lighting (paragraph

S.a)

and

the violations identified below.

Si nificant Safet

Matters:

None

Summar

of Violations:

One Severity Level

IV violation was identified,

involving the loading of two one-ton chainfalls to approximately

2400

pounds

each wile installing

a resin cask lid (paragraph 3.b(2)).

Two

non-cited violations were also identified, involving inconsistent

fastener torques for two residual

heat

removal

(RHR) system valves

(paragraph

S.b)

and failure to declare

a Unit 2 main steam safety valve

inoperable after test equipment

used to establish its setpoint

was found

to have failed (paragraph

10.k).

en Items

Summar

Three

new followup items were opened.

Ten followup items were reviewed;

9 were closed, I remains

open.

Twenty LERs were reviewed;

19 were

closed,

1 remains

open.

Persons

Contacted

acific Gas

and Electric

Com an

G. H. Rueger,

Senior Vice President

and

General'anager,'uclear

Power Generation

Business

Unit

J.

D. Townsend,

Vice President

and Plant Manager,

Diablo Canyon

Operations

W. H. Fujimoto, Vice President,

Nuclear Technical

Services

D. B. Miklush, Manager,

Operations

Services

  • H. J. Angus,

Manager,

Technical

Services

  • B. W. Giffin, Manager,

Maintenance

Services

  • W. G. Crockett,

Manager,

Support Services

~J.

E. Molden, Instrumentation

and Controls Director

  • W. D. Barkhuff, guality Control Director
  • R. P.

Powers,

Mechanical

Maintenance Director

T. L. Grebel,

Regulatory Compliance Supervisor

H. J. Phillips, Electrical Maintenance Director

  • J. A. Shoulders,

Onsite Project Engineer

  • S. R. Fridley, Operations Director
  • R. Gray, Radiation Protection Director

J. J. Griffin, Senior Engineer,

Regulatory Compliance

J.

V. Boots,

Chemistry Director

  • T. A. Moulia, Assistant to Vice President,

Diablo Canyon Operations

  • R. Kohout, Safety,

Health

and

Emergency Services Director

  • D. P. Sisk, Regulatory Compliance

Engineer

D.

R. Stermer,

Power Production

Engineer

M. R. Tresler,

Project Engineer

R. Clark, Assistant Project Engineer

R. Gagne, Acting Radwaste

Foreman

U. A. Farradj, Fire Protection

Engineer

R. A. Waltos, Senior

Power Production

Engineer

S.

F. Shrefler,

Mechanical

Maintenance

Engineer

B. D. Pogue,

System Engineer

R. Ortega,

System Engineer

R. Watson, guality Assurance

Engineer

San Luis Obis

o Count

Officials

R. Hendrix, Administrator

L. Williams, Deputy Administrator

V. Horici, Emergency

Response

Coordinator

  • Denotes those attending the exit interview.

The inspectors

interviewed several

other licensee

employees

including

shift supervisors,

shift foremen

(SFH), reactor

and auxiliary operat'ors,

maintenance

personnel,

plant technicians

and engineers,

and quality

assurance

personnel.

2.

0 erational

Status of Diablo Can

on Units I and

2

Dunng the )nspectson

period,

Unst I operated

at

IOOX power, except for

April 25-27,

and Hay 2-3,

1992.

On April 25, Unit I reduced

power to 50X

for routine condenser

cleaning.

While conducting maintenance

on the l-l

main feedwater

pump,

vacuum in the condenser

was lost, causing the main

turbine

and the reactor to trip.

Unit I was restarted

on April 26 and

was at full power on April 27.

This .event is described in paragraph

4.a

below.

During the period Hay 2-3,

1992, Unit I was curtailed to 50X

power for routine condenser

cleaning.

Unit 2 operated

at

100X power during the reporting period.

3.

0 erational

Safet

Verification

71

07

a.

General

During the inspection period, the inspectors

observed

and examined

activities to verify the operational

safety of the licensee's

facility.

The observations

and examinations of those activities

were conducted

on a daily, weekly or monthly basis.

On a daily basis,

the inspectors

observed control

room activities to

verify compliance with selected

Limiting Conditions for Operation

(LCOs)

as prescribed

in the facility Technical Specifications

(TS).

Logs, instrumentation,

recorder traces,

and other operational

records

were examined to obtain information on plant conditions

and

to evaluate trends.

This operational

information was then evaluated

to determine whether regulatory requirements

were satisfied.

Shift

turnovers

were observed

on

a sample basis to verify that all perti-

nent information on plant status

was relayed to the oncoming crew.

During each

week, the inspectors

toured accessible

areas of the

facility to observe the following:

(I)

General

plant and equipment conditions

(2)

Fire hazards

and fire fighting equipment

(3)

Conduct of selected activities for compliance with the

licensee's

administrative controls

and approved

procedures

(4)

Interiors of electrical

and control panels

(5)

Plant housekeeping

and cleanliness

(6)

Engineered

safety features

equipment alignment

and conditions

(7)

Storage of pressurized

gas bottles

The inspectors

talked with control

room operator s and other plant

personnel.

The discussions

centered

on pertinent topics of general

plant conditions,

procedures,

security, training,

and other aspects

of the work activities.

-3-

The inspectors

also

accompanied

auxiliary operators

during their

rounds in the plant and reviewed the associated

log entries.

On two

occasions

the inspector verified that auxiliary operators

were

completing their rounds consistent with the -log sheet entries.

No

instances

of improper log entries

were identified.

b.

Radiolo ical Protection

(1)

The inspectors periodically observed radiological protection

practices to determine

whether the licensee's

program was being

implemented in conformance with facility policies 'and proce-

dures

and in compliance with regulatory requirements.

The

inspectors verified that health physics supervisors

and

professionals

conducted

frequent plant tours to observe

activities in progress

and were aware of signi'ficant plant

activities, particularly those related to radiological

conditions and/or challenges.

ALARA considerations

were found

to be

an integral part of each

RWP (Radiation

Work Permit).

(2)

Radioactive

Waste Shi ment on Ha

28-29

1992

The inspectors

observed

the licensee's

preparation to ship

a

high integrity container

(HIC) of radioactive resin to

Richland,

Washington for disposal.

The licensee

planned to

survey

and

remove the HIC from storage

in a permanent

plant

shield cask

and place the HIC in a transportation

cask carried

on

a sole-use

flatbed truck.

A shielded

boom crane

was

used

for this movement.

The evolution was significant in that it

occurs infrequently

(1 to 2 times

a year at most)

and the

HIC

had

a surface

dose rate of over 30 R/Hr.

The inspectors

observed

the licensee's

pre-brief meeting which covered

communications,

surveys,

exclusion areas,

ALARA considerations,

crane operations,

and contingency plans.

The inspectors

observed

the HIC transfer,

which proceeded

without incident.

However,

when placing the lid on the

shipping cask,

licensee

personnel

were initially unable to get

it to seat properly.

The lid was supported

by three slings

and

restrained horizontally with respect to the cask by two guide

pins.

With the lid resting

on the top of the cask,

the

licensee's

riggers replaced

two of the slings with chainfalls.

This allowed the lid to be leveled

by an individual standing

on

top of the lid and adjusting the chainfalls.

The rigger

leveling the lid was shielded

from the

HIC by the lid itself.

The lid was approximately

3 inches higher than the seated

position during the evolution.

After several tries the lid

seated

and the rigging equipment

was removed.

During this evolution, the inspector questioned

licensee

personnel

as to whether the chainfalls being used

had adequate

capacity.

The licensee

personnel

present

stated that they were

confident that the riggers

knew what they were doing.

The

inspector stated that the chainfalls looked like one-ton units

and the cask lid looked substantially heavier.

i

The next day,

Hay 29,

1992, the inspector conducted

a survey of

the shipping cask

on the truck.

Radiation levels

appeared

to

be, within regulatory limits and the cask appeared

to be proper-

ly secured

and labeled for shipment.

The inspector

observed

that the weight of the cask lid was approximately

7300 pounds.

The inspector discussed

the chainfall.capacity. with the Mecha-

nical Haintenance

Director

who determined that the chainfalls

used

had

been one-ton units.

The licensee's

quality evaluation

found them to have

a safe working load of 2000 pounds

each.

The load on each chainfall would have

been approximately

2400

pounds.

The inspector

noted that this was

a personnel

safety

issue

and that the individual standing

on the cask lid could

have

been seriously hurt if the chain

had parted.

The Manager

of Maintenance

Services

and Mechanical

Maintenance Director

agreed that

a mistake

had

been

made.

Licensee

personnel

stated

that when the next shipment

was

made the correct size chain-

falls would be available

and 'that their use would be required

by written instructions.

This,is an apparent violation of

Technical Specification 6.8.1

and procedures for control of

rigging and load handling equipment.

(50-275/92-16-01)

The inspector

observed that this event involved riggers'and

contained

elements similar to the loss of offsite power event

in March 1991 which was caused

by a boom crane

under the Unit

1

500KV lines.

The Manager of Maintenance

Services

stated that

the

boom crane event in 1991

had

been

caused

by personnel

who

were not riggers,

but who had been trained to use the equip-

ment.

The inspector

acknowledged that two different groups of

personnel

were involved, but noted that both events

appeared

to

involve weakness

in the preplanning

and control of lifting or

rigging activities.

c.

Ph sical Secur't

Security activities were observed for conformance with regulatory

requirements,

the site security plan,

and administrative procedures,

including vehicle

and personnel

access

screening,

personnel

badging,

site security force manning,

compensatory

measures,

and protected

and vital area integrity.

Exterior lighting was checked during

backshift inspections.

No violations or deviations

were identified.

4.

Onsite Event Followu

93702

a ~

Tri

of Unit

1

Due to Loss of Vacuum on

A ril 25

1992

Between 9:00 p.m and 11:00 p.m.

on April 24,

1992, plant operators

decreased

Unit

1 power to approximately

50X to allow routine

cleaning of the east

main condenser

water boxes.

Main feedwater

pump

(HFP) l-l was shut

down and cleared to make repairs to

steam'top

valves to the

MFP turbine.

At approximately 3:45 a.m;,

vacuum in the operating

west condenser

had degraded

to an absolute

pressure of approximately 4.5 inches

Hg.

The air in-leakage

which degraded

condenser

vacuum was apparently

due to leakage

through the large l-l MFP exhaust butterfly valve.

The on-shift crew attempted to stop the air in-leakage

by reseating

the closed

1-1

HFP exhaust

valve and by placing

a second air ejector

in service.

At 4:00 a.m., plant power was. being decreased

at

10

NW

per minute

and gland seal

steam

was re-established

to the

HFP 1-1

turbine.

The decrease

in power appeared

to be helping condenser

vacuum.

At 4:07 a.m., plan+operators

attempted to place the Nash

mechanical

vacuum

pump in service.

When the vacuum

pump suction

valve from the west main condenser

was opened,

backpressure

increased

rapidly and at 4:08 a.m.

a turbine trip and reactor trip

occurred.

The operators

subsequently

stabilized the plant in

accordance

with Emergency Operating

Procedures.

All safety related

equipment functioned

as expected.

At 5:10 a.m.,

the licensee

made

a

four hour non-emergency

report to the

NRC.

The inspector evaluated

the licensee's

investigation,

discussed

the

event with the on-shift crew,

and observed

the subsequent

plant

startup.

At approximately

1:00 p.m.

on April 27, after evaluation

of the event

and correction of the cause of the trip, the licensee

restarted

Unit 1.

The startup

was uneventful

and Unit

1 returned to

full power the morning of April 28,

1992.

The inspector

observed that the licensee's

investigation into the

trip identified the following information:

After the operators

had

begun to reduce

power at

10

HW per

minute,

condenser

vacuum was stabilizing.

The problem may have

corrected itself without further action.

Placing the

Na'sh mechanical

vacuum

pump in service

was

consistent with the licensee's

procedure

AP-7, "Loss of

Condenser

Vacuum".

However,

AP-7 did not contain the specific

steps

necessary

to place the Nash

pump in service.

The operators

in the turbine building at the Nash

pump did not

have

a local copy of the procedure to place the

pump into

service.

Due to the sense of urgency the operators

in the

control

room did not review the procedure to place the Nash

pump in service.

Unknown to the operators,

a seal

water isolation valve for the

Nash

pump was required to be opened

before the

pump could

operate properly.

When the suction valve to the west condenser

was opened, air entered

the condenser

through the

Nash

pump

seals.

The condenser

vacuum

pump suction check valve appears

to have

leaked severely in the reverse direction, allowing air flow

back to the condenser.

The inspector discussed

the event with the Operations Director to

determine the adequacy of the licensee's

corrective actions.

The

licensee

issued

an Incident Summary to alert other crews

and

added

precautions

to be taken in the procedure for shutdown

and clearing

of a main feedwater

pump.

The licensee

plans to inspect

each unit's

vacuum

pump suction line check valve during outages

1R5 and

2R5.

The licensee

also plans to complete

a review of all emergency

and

abnormal

operating

procedures

to identify situations in which opera-

.

tors might be dispatched

to perform equipment operation without

procedures.

By September

1,

1992, controlled local procedures

or

postings

are planned to be aided

based

on the review.

The inspector questioned

the adequacy of the licensee's

preparation

for taking

HFP l-l out of service.

Licensee

personnel

stated that

preparations

had been

adequate,

but that the plant had not responded

as expected.

This event

was described

in Licensee

Evqnt Report

(LER) 1-92-004,,issued

May 22,

1992.

The inspectors will followup

the licensee's

analysis of the event

and corrective actions during

review of the

LER.

No violations or deviations

were identified.

5.

Maintenance

62703

The inspectors

observed portions of,

and reviewed records

on, selected

maintenance activities to assure

compliance with approved

procedures,

Technical Specifications,

and appropriate

industry codes

and standards.

Furthermore,

the inspectors verified that maintenance activities were

performed

by qualified personnel,

in accordance

with fire protection

and

housekeeping

controls,

and that replacement

parts

were appropriately

certified.

These activities included:

Work Order No. C0096441,

BATP1, Replace

Mechanical

Seal

Work Order No. C0100168,10-142,

Cask,

Provide Support to Hove Cask

a.

Concerns

Raised

Durin

Observation of Boric Acid Transfer

Pum

aintenance

During an observation of Work Order

No C0096441,

BATPl, "Replace

Mechanical Seal," the inspector

noted the following concern:

(1)

When questioned

by the inspector,

the mechanics

performing

alignment of the

pump and motor coupling stated that guality

Control sign-off of the alignment would require removal of the

optical alignment tool used to align the coupling,

and instal-

lation of a double dial indicator,

an older, slower alignment

tool.

This was required

because

guality Control would not rely

on optical alignment information.

Further review by the inspector

and Mechanical

Haintenance

management

found that guality Control

had accepted

optical

alignment information a few months

ago,

but that the Mechanical

Maintenance

foreman

and mechanics

had not all been

informed.

Although both alignment methods

are valid, the inspector

was

concerned that the mechanics

and foreman were not informed of

processes

which could reduce radiation exposure

by reducing

time in radiation fields.

The licensee is reviewing training

and technical

information provided to foremen to determine if

timely and adequate

information is provided to Mechanical

Maintenance

foremen.

(2)

The work order required all workers to attend the tailboard

discussion.

However, tge mechanic performing alignment of the

pump and motor coupling had not attended

the tailb'oard.

The

licensee

stated that coupling alignment activities are highly

specialized,

and in this case did not require attendance

of the

tailboard, in that the mechanic

had

been briefed

on the job and

provided adequate

information to perform the work safely.

The

inspector

noted that the procedure

requirements

qnd expecta-

tions for specialists

regarding tailboard attendance

were not

specific,

and

may be subject to incorrect interpretation,

par-

ticularly during times of high work activity such

as

an outage.

The licensee

was planning to review expectations

regarding

attendance

at tailboards

before the next scheduled

outage.

These

issues will be followed during routine resident inspection

activities.

No violations or deviations

were identified.

~

~

~

~

~

~

lj

6.

Surveillance

61726

By direct observation

and record review of selected

surveillance testing,

the inspectors

assessed

compliance with TS requirements

and plant

procedures.

The inspectors verified that test equipment

was calibrated,

and that test results

met acceptance

criteria or were appropriately

dispositioned.

These tests

included:

STP I-18W2D, Revision 5, Isotopic Calibration of Plant Vent Mid

Range

Iodine Radiation Monitor RH-32

STP R-3A, Use of Flux Mapping Equipment (Unit 2)

STP H-IIB, Measurement of Station Battery Voltage and Specific

Gravity (Unit I)

STP M-45B, Containment

Inspection

When Containment Integrity is

Established

(Unit 2)

STP H-51A, Routine Surveillance of Containment

Fan Cooler Unit

(CFCU) for Reverse

Rotation

(CFCU 2-4)

'a Q

STP

I-18W2D

Revision

5

Isoto ic Calibration of

lant Vent Mid

Ran

e Iodine Radiation Monitor RM-32

During review of this surveillance activity, the licensee

noted that

several

Instrumentation

and Control

(I&C) calibrations

had

been

performed during the TS grace period

(25X beyond the surveillance

interval specified in the TS).

The inspector

was informed by IKC

technicians that routine use of the grace period was beiag stopped

by management,

and that surveillance activities have more recently

been

and will in the future continue to be performed within the

TS

inte>val.

This effort was documented

in problem identification

document

qE No. 9766, dated

Hay 27,

1992.

The inspector

reviewed

a

sample of recent

18C surveillances,

and found that more recent sur-

veillance tests

had been

accomplished within the

TS interval, rather

than during the grace period~

as

was the case for some surveillance

activities performed

more than six months

ago.

This licensee

initiative was noted

by the inspector to reflect

a more conservative

approach to the scheduling of surveillance activities.

b.

Pro

ram to

U

rade Radiatio

onitor Cal bration Procedures

The inspector

observed

implementation of a review of radiation

monitor calibration procedures

to identify vague or conflicting

guidance.

The licensee

had identified this effort in an action plan

and several

action requests.

The review and associated

effort

appeared

appropriate.

Followup of this effort will be performed

as

part of routine resident

inspection of surveillance activities.

No violations or deviations

were identified.

En ineerim

Safet

Feature Verificatio

71710

During the inspection period, selected

portions of the safety injection

system for Units

1 and

2 were inspected to verify that system configura-

tion, equipment condition, valve and electrical lineups,

and local

breaker positions were in accordance

with plant drawings

and Technical

Specifications.

No violations or deviations

were identified.

8.

Exam les of Inade uate

Problem Identif'cation

a.

lant Construction

Obscures

10 CFR 50

A

endix

R

Li htin

In Unit 1, Buses

G and

H switchgear

rooms, construction

work is

underway to strengthen

masonry walls.

In both rooms,

a plastic tarp

was

hung from floor to ceiling along the length of one wall to pro-

tect the switchgear

from debris

gener ated

by the constr uction work.

On Nay 19,

1992, the inspector

noted that the Appendix

R emergency

lighting for both rooms

was covered

by the tarps.

Emergency light-

ing is installed in the

4KV switchgear

rooms to provide lighting for

operator actions in the event of a fire.

Operator actions

are docu-

mented in procedures

OP-AP-8A and

B, Control

Room Inaccessibility,

and

EP H-10, Fire Protection of Safe

Shutdown Equipment.

The licensee

documented

the problem in AR No. 266808,

and replaced

an approximately

6 ft by 5 ft square

section of the plastic in front

nf the lights with transparent

plastic.

The licensee

was planning

to evaluate operability of the lighting, and assigned

system

engineering responsibility for Appendix

R lighting to the fire

protection

and emergency

services organization.

Appendix R,Section III.J, requires

emergency lighting in all areas

needed for operation of safe

shutdown equipment.

The operability of

the lighting, and root cause of the failure to identify and correct

the problem until noted

by the inspector, will be followed as

Unresolved

Item 50-275/92-16-02.

Contradictor

Tor ue Docume

ation for Residual

Heat

Removal

RHR

S stem Valves

During review of the evaluation section of Action Request

No.

230770,

which identified recent indication of leakage

from Unit

1

valve

RHR 8702, the inspector noted that

a second

problem was dis-

cussed

concerning evaluation of inconsistent

torque documentation.

Torques of 1500 and

2500 ft-lbs for bonnet fasteners

were listed in

separate

reference

documents.

This inconsistency

was not identified

in a separate

Action Request

as required,

and therefore

may not have

been

reviewed by guality Assurance.

After the inspector identified

the issue,

the licensee

acknowledged that the lack of a separate

problem identification document

was inappropriate,

and initiated

a

second Action Request

(267237) to identify the problem.

The inspector

was concerned that,

based

on inconsistent

information,

fasteners

with incorrect torque

may have

been installed in the

plant.

Licensee investigation determined that the valve manufac-

turer initially recommended

1500 ft-lbs, but had later offered

different valve trim designs.

The manufacturer

then specified

2500

ft-lbs torque because it bounded all design options for this valve

line,

and documented this value in later vendor manuals.

Recent

vendor correspondence

validated this assessment.

Installation

records

from 1973 for original design valves

showed torques of 1800

ft-lbs, which the licensee

considers

an acceptable

torque value.

Additionally, the licensee

stated that these

valves are specifically

inspected for boric acid leakage at least every outage during sur-

veillance test

STP R-BC, Containment

Malkdown for Evidence of Boric

Acid Leakage, to comply with the licensee's

response

to Generic Letter 88-05 concerning boric acid corrosion of fasteners.

Because

no leakage

has

been previously observed,

the licensee

concluded that

this is further assurance

that fastener

torque is adequate.

The licensee

stated that this issue

had not been identified in the

past

because

no work had

been performed

on the two val.ves of

concern,

RHR 8701

and 8702, since original installation.

The failure to promptly identify a problem adverse

to quality is

considered to be

a violation of 10 CFR 50, Appendix B, Section XVI.

Because

the torque inconsistencies

did not appear to be safety

significant,

and because

licensee corrective actions

were prompt,

this violation is not being cited because

the criteria specified in

Section V.A. of the Enforcement Policy were satisfied.

(NCV 92-16-03, 'Closed)

1

e

10

i

c.

Uncontrolled Information in Electrical

Panels

During routine inspection activities, the inspector

observed

uncontrolled,

outdated,

and in some cases

inaccurate

drawings

and

circuit lists attached to the inside of several electrical

breaker

panels.

The presence

of uncontrolled information in electrical

panels,

particularly in Cl.ass

1 panels,

was of concern.

After

discussion

with the inspector,

the licensee

determined that this

information was inconsistent with the requirements

of Administrative

Procedure

AP C-55,

and indicated lack of a formal program for

updating electrical labels

a% part of the design process.

Licensee

work control

and operations

procedures

requ'ire

use of controlled

drawings

and information for work associated

with these

panels.

Inspector observations

indicated that the existence of these

uncontrolled drawings did not appear to have

encour'aged

the licensee

to circumvent the use of controlled drawings.

Therefore,

the safety

significance of uncontrolled drawings in panels

appeared

low.

Removal of uncontrolled information from inside electrical

panels

will be followed by routine inspection activities.

One non-cited violation was identified (paragraph 8.b).

9.

Potential

Weakness

in Understandin

the Recircu at'o

P ase

Desi

n

s

s

In recent months,

the inspector

has noted the occurrence

of five issues

which appear to have

been partially caused

by insufficient awareness

of

design basis

requirements for the

ECCS recirculation phase.

They are

as

follows:

~

Diaphragm Valve Leakage

May Have Exceed Part

100 Limits (LER 50-323/

92-09).

~

Charging

Pump

and Safety Injection

Pump Runout Limits Exceeded

(NCR-

DC0-92-NS-N007).

~

Leakage

Path Vulnerability Via Volume Control Tank (VCT) Outlet

Check Valve (LER 50-275/92-01).

~

Inaccurate

Single Failure Analysis Allows the Possibility that

Com-

ponent Cooling Mater

(CCW) Heat

Load may Incr ease,

and Charging

Pump

Bearing Temperature

Limits may be Exceeded

(LER 50-275/91-18).

~

Inaccurate

Single Failure Analysis Allows the possibility that

Long

Term Containment

Temperature

Profile Assumptions

may be Exceeded

due

to Lack of Containment

Spray

(NCR DC0-92-EN-N002).

The inspector identified to the licensee that these

issues

may indicate

insufficient understanding

and integration of ECCS recirculation

phase

design requirements,

with the potential for additional safety issues

which have not yet been identified.

The licensee

agreed to consider

and

evaluate this possibility.

The licensee identified that this may be

a

generic Westinghouse

design issue,

and was planning to explore this issue

with the Westinghouse Owners'roup.

Followup of the licensee's

evaluation will be tracked

as Followup Item 50-275/92-16-04.

~

~

10.

Licensee

Event

Re ort Fol

owu

92700

a.

Unit I Control

Room Ventilation

S stem Outs'de

esi

as's

LER 50-275 83-39

Revision

0

C osed

On November 21,

1991, the licensee identified that the control

room

ventilation system could be outside its design basis

as

a result of

a single failure of a booster fan or its associated

damper.

The

fans are positioned in parallel flow paths,

and failure would allow

unfiltered air into the consol

room during the pressurization

mode.

As a temporary corrective measure,

the licensee

issued

Operations

Department night orders to the control

room discussing

the vulnera-

bility, and installed flow indicators

on ducts in the control

room.

The licensee

also changed

emergency

operating

procedures

to require

verification that flow is occurring in the proper direction through

the ducts

by observing the flow indicators.

The licensee

has prepared

and scheduled

a design

change to provide

permanent resolution of the vulnerability.

Therefore, this item is

closed.

b.

Unit I Check Valve Inservice Testin

eficiencies

R 50-2

5 84-4

evisio

Closed

!

C.

As a result of deficiencies

in the check valve inservice testing

(IST) program,

two additional valves were identified which require

testing in the closed direction.

Identification of these

valves

occurred after review of a Westinghouse

Information Letter dated

August 4,

1989.

The valves,

HS-5166

and -5177,

are in the steam

supply lines to the turbine driven auxiliary feedwater

(AFW) pump.

Testing

was in place to verify the valves

opened to supply steam

when required,

but not that the valves closed in order to prevent

an

intact steam generator

from blowing down through the

AFW pump steam

supply line to containment after

a main steam line break.

The

NRC

approved

a relief request to allow the licensee to disassemble

and

inspect the valves

on

a rotating refueling outage

frequency.

The

licensee

has

added this testing

and inspection requirement to the

IST program.

This item is therefore closed.

Unit I Emer enc

Diesel Generator

EDG l-l Failure to Start

S ecial

Re ort 50-275 89-01

Revisions

1 and

2

0 en Item 89-Ol-XO

Closed

On February I, 1989, during

a routine surveillance

procedure,

EDG

l-l failed to start.

Two of the four air start motors failed as

a

result of overload of the pinion retainers,

pinion retainer bolting

and rotor shafts.

The licensee

entered

TS action statements

corresponding

to an inoperable diesel generator,

and

commenced

investigation

and repair.

The licensee attributed the cause of the

failure to inadequate fit-up of the pinion gear

and rotor shaft

during plant maintenance,

resulting in improper torque transmittal.

The licensee identified several

possible contributory causes,

including excessive

Train "A" starting air pressure,

improper vendor

-12-

tolerances for slot fabrication of the pinion retainer,

inadequate

vendor assembly instructions for the motor,

and

an inadequate

pinion

retainer bolt locking mechanism.

Revision

1 of this special

report

provided inspection results for the remaining

18 air start motors,

which identified

11 additional air motors with incorrect fit-up and

10 with rotor cracks.

The licensee

documented corrective action for each of the above

listed causes,

and performed engineering

analysis of the design of

the diesel air start configugation.

The licensee

concluded that the

air start

system

was adequate

and, in conjunction with 'corrective

actions,

was acceptable.

The licensee

discussed

their findings with the vendor.

The vendor

indicated that they were not aware of any similar failures.

The

licensee

informed other licensees

of their findings through

an

industry problem communications

system.

This issue

was also the

subject of NRC Information Notice 89-84.

The above actions

appeared

appropriate

This item is closed.

'Unit

1 Fuel Handlin

Buildin Ventilation I o crab

e

Ou in

Fue

Movement

LER 50-275 89-

9

Revision

1

Closed

On, January

18,

1991, the Unit

1 fuel handling building failed to

meet the negative I/8-inch water gage pressure

acceptance

criterion.

The licensee

determined that the fuel handling building ventilation

system

had

been inoperable

since October

15,

1989,

when fuel

movement occurred during the Unit

1 third refueling outage.

Investigation of the root cause of failure identified sources of

leakage to be gaps in sheet

metal siding, unsealed

piping

penetrations,

missing or degraded

door seals,

gaps

between

the

movable crane wall and the fixed walls, through-wall oxidation of

sheet

metal siding,

and reduced flow through the ventilation ducts

due to accumulation of debris.

Because

sealing of the pressure

boundary provided adequate

negative pressure,

the root cause

was

considered

to have

been degradation of the building seals.

P

Based

on observation of the implementation of the design

changes

on

the fuel handling building seals,

and licensee

action which has

maintained continuing awareness

of fuel handling building

ventilation operability, this item is closed.

Ino erable Unit

1 Valve Due to Limitor ue

S rin

Pack Relaxation

LER 50-275 90-09

Revision

0

Closed

In March,

1990, during overhaul of a safety injection system valve,

a spring pack for a motor operator

was found to have

a less than

expected preload.

This condition was also identified on two other

valves,

and was verified to be the result of spring pack degra-

dation.

Nine valves in each unit were identified as potentially

affected.

In May 1990, the vendor,

Limitorque, issued

a Maintenance

Update Bulletin which indicated that valve models other than

SMB-0

-13-

may also have spring pack. relaxation.

After review of maintenance

records

and valve diagnostic information, the licensee

determined

that no additional valves were affected at Diablo Canyon.

The

licensee

replaced

each of the potentially affected springpacks,

and

evaluated

the safety significance of the spring packs which had been

identified as degraded.

Based

on the

as found evaluation,

the

licensee

concluded that the affected valves would have performed

their safety function.

Based

on this assessment

and the prompt

corrective action, this item is closed.

Failure to Perform Houri

Un t

Fire Watch

LER 50-

5'

-15

Revision

0

Closed

On September

17,

1991,

a roving hourly fire watch was not performed

in some of the safety related

equipment

rooms.

The fire watch was

delayed leaving the radiologically controlled area,

aqd was not able

to contact his supervisor in time to prevent violation of the

Technical Specification requirement.

For corrective actions,

an incident summary

was prepared

and

reviewed with fire watch personnel,

and included in fire watch

training.

Written instructions

have

been provided to personnel for

actions to take if delays occur on rounds.

Therefore this item is

closed.

Ino erable Unit

1

EDGs While Fuel

Pool

Crane

Was 0 e at

Over

uel

Pool

LER 50-275 91-14

Revision

0

Closed

On February

13,

1991, with the core offloaded, all three

EDGs

became

inoperable.

During this time, irradiated fuel was moved in the

spent fuel pool.

Although

a specific operational

mode was not in

force, the licensee

determined that the intent of TS 3.8.5.2.b.

(Electrical

Power Requirements)

was not met, since loss of offsite

power would have resulted in loss of fuel handling building venti-

lation.

The licensee

returned

EDG 1-2 to service

on February

13.

For corrective action, the licensee

issued

procedural

guidance to

interpret electrical

power requirements

to include operational

conditions

when the core is offloaded.

This corrective action

appeared

appropriate.

This item is closed.

Hissed

Rod Position Indication Surveillance

Unit

1

LER 50-275

91-17

Revision

0

Closed

From November

14 to November

16,

1991,

rod position surveillance

tests

were missed

as

a result of inadequacies

in the plant process

computer

(PPC) software.

After the

PPC was shut

down and restarted

on November

14, the

PPC incorrectly updated

the reactor trip

breakers'tatus

as open.

Therefore,

the logic in the

PPC inhibited

the alarm function of the rod position deviation monitor.

Licensee

corrective actions included assessment

that rod position had

been

correct during the interval of missed surveillance,

revision of the

PPC software,

operator training to identify rod position deviation

monitor inoperability,

and revision of procedure

AP C-27,

Computer

Software guality Assurance,

to ensure significant computer functions

-14-

are verified on an appropriate

schedule.

These actions

appeared

appropriate,

and this item is closed.

Unit I Low Vacuum Turbine Tri

and Subse

uent Reactor r'ue to a

Pro rammatic Deficienc

LER 50-275 .92-04

evision

0

0 en

This event is described

in paragraph

4.a of this report.

The

LER

will be left open for followup of licensee'orrective

actions

related to posting local procedures.

Ino erable Unit 2 Fuel Handlin

Buildin Ventilation

S stem

urin

Fuel

Movement

LER 50-323 90-02

evision

2

Closed

As a result of inadequate

planning

and understanding

of fuel

handling building ventilation system operability requirements,

the

licensee

moved fuel in the spent fuel pool while the fuel handling

ventilation boundary doors were blocked

open with temporary

hoses

used for outage work.

As

a result, the required negative pressure

was not adequately

maintained.

The licensee

reviewed this event

with Operations

and Maintenance

personnel,

and posted

signs

on all

affected doors

announcing

the need to ensure that doors are closed

during fuel movement.

This corrective action appeared

adequate;

therefore, this item is closed.

Corrective action for the generic

concern of personnel

errors will

be addressed

in Followup Item 50-275/91-27-02,

documented later in

this report.

This item is therefore closed.

Two Unit 2 Main Steam Safet

Valves Set With Ino erable

est

E ui ment

LER 50-323 91-02

Revi sip

0

C osed

On August 26,

1991, the licensee

performed routine verification of

main steam safety valve setpoints.

After two valves were adjusted,

it became

apparent that the test equipment

had failed.

First,

FV-60

had been adjusted

+3 flats, roughly a 33 pounds per square

inch

(PSI)

change in setpoint.

Then,

RV-225 had been adjusted

13 flats,

roughly corresponding

to 143 psi setpoint

change.

Because of the

unexpectedly

high magnitude of adjustment,

the licensee

suspected

and promptly confirmed improper performance of the test equipment.

Valve RV-225 was declared

inoperable.

However, the licensee

did not

declare valve RV-60 inoperable,

based

on the small,

expected

magni-

tude of adjustment.

Subsequent

testing

found that RV-60 lifted

4 psi

above its +/- 1X tolerance

range.

The licensee

concluded that the test equipment

had failed abruptly

while setting

RV-225,

and

had

been operable while setting

RV-60.

The licensee

also concluded that there

was

no firm evidence that the

test equipment

caused this out-of-tolerance setpoint for RV-60,

since setpoint drift is

common

and expected

up to +/-3X.

Because

RV-60 was not declared

inoperable after test equipment failure was

confirmed, the

NRC concluded that this was

a non-cited violation

(50-323/91-24-02),

based

on the low safety significance of the

as

found setpoint of RV-60, the licensee's

prompt corrective action to

fix the test equipment

and validate the actual safety valve set-

-15-

points,

and continuing improvement in documentation of the rationale

for operability decisions.

Therefore, this item is closed.

Inadvertent

Removal of Power

From Unit 2

RHR

Pum

Sum

Suction Valve

0 erators

Before Enterin

Mode

5

LER 50-323 91-03

ev sion

0

Cl osed

On September

1,

1991, control

room operators

determined that both

RHR sump suction valves

and both containment

spray

(CS)

pumps were

inoperable.

The

RHR valve breakers

had

been

opened locally, and

control power to the

CS pump breakers

had been

removed;

Both

events'ccurred

after entry into hot shutdown earlier in the day,

and were

corrected within 15 minutes after identification by operators.

For the

RHR valves,

power must

be removed from the 'Valves at the

control

room contactor toggle switches

(rather than the local

breakers)

to satisfy safety analysis

requirements

that power be able

to be restored

from the control

room.

Procedure

OP L-5 required

power be removed from the valves at the local breaker,

thus

violating safety evaluation requirements.

The licensee

revised

OP

L-5 and reviewed all other L-series procedures.

For the Containment

Spray pumps,

power was removed before entry into

Mode

5 as

a result of inadequate

control

and review of clearances

by

a Senior Control Operator.

Specific licensee corrective actions

included issuing

an Operations

Incident Summary

and memoranda

stressing

the significance of this

event

and the need for ensuring

TS commitments

are met.

Corrective

action for the generic concern of personnel

errors will be addressed

in Followup Item 50-275/91-27-02,

documented later in this report.

This item is therefore closed.

Shift of Unit 2 Control

Room

Ve tilation Mode

LER 50-323 91-06

Revision

0

Closed

On October 3,

1991,

an inadvertent

engineered

safety features

(ESF)

actuation occurred.

This was the result of inattention to detail

by

two operators

who lifted an incorrect lead while attempting to

remove

an inverter from service.

Power was interrupted to inverter

IY-23, resulting in a shift of the control

room ventilation system

to the pressurization

mode.

All safety systems

functioned

as

expected;

The operators

followed generic procedure

guidance

instead of

detailed information provided in an attachment.

As corrective

action,

both operators

were counseled

regarding attention to detail,

and the procedure

was revised to delete the generic steps

and

emphasize

detailed information.

Corrective action for the generic

concern of personnel

errors will be addressed

in Followup Item

50-275/91-27-02,

documented later in this report.

This item is

therefore closed.

0

-16-

Inadvertent Unit 2 Safet

In'ection While in Mode

5

LER 50-323 91-

07

Revision

0

Closed

On October 6,

1991, during a refueling outage

(Mode 5), technicians

inadvertently caused

a safety injection signal

by performing

protection switch positioning out of the correct

sequence.

The

cause of the event

was inattention to detail.

All expected

ESF

actuation

signals occurred.

No water was injected into the core,

since

emergency

core cooling pumps were secured for maintenance.

The technicians

were counsel1ed

according to the licensee's

positive.

discipline program,

and

a memorandum

was is'sued

by the Plant Manager

emphasizing

the need for procedure

compliance

and verification.

Corrective action for the generic

concern of personnel

errors will

be addressed

in Followup Item 50-275/91-27-02,

documented later in

this report.

This item is therefore closed.

Unit 2 Valve Leaka

e

Ma

Have Resulted

in Exceedin

10 CFR 100 Doses

LER 50-323 91-09

Revisions

0 and

1

Closed

On October 4,

1991,

1.3 gallons per minute leakage

from diaphragm

valves

CVCS-2-8471

and -548 was evaluated

by the licensee.

The

evaluation

concluded that the control

room and exclusion area

boundary

10 CFR 100 limits could have

been

exceeded

during the

recirculation

phase of a loss of coolant accident

(LOCA).

The licensee

determined that the diaphram service life for CVCS-2-

8471

had

been

exceeded

and that diaphram degradation

had resulted in

leakage.

The

LOCA analysis

had not identified CVCS-2-8471

as

a

valve in the recirculation

phase flow path.

As a result,

the valve

was not included in the licensee's

preventive maintenance

program

for diaphragm replacement.

The licensee

determined that the body-to-bonnet bolts for CVCS-2-548

had not been retorqued at normal operating pressure

and temperature

following maintenance,

as

was required for that type valve.

The

licensee

committed to revise the procedure to include this step.

While this specific issue is closed,

the inspector

was concerned

that other issues

concerning the design requirements

of the

recirculation

phase

may not have

been adequately

addressed,

and

documented

the need for

NRC followup of this concern earlier in this

report.

Ino erable Unit

1 Wide Ran

e Containment

Sum

Level Indicatio

LER 50-323 91-10

Revisions

0 and

1

C osed

On October 22,

1991, with Unit 2 in Mode

2 at

OX power,

TS Action

Statement

3.3.3.6

was exceeded

due to the reactor cavity sump wide

range level channel

being inoperable for more than

seven

days.

The

channel

was returned to service

about

7 hours8.101852e-5 days <br />0.00194 hours <br />1.157407e-5 weeks <br />2.6635e-6 months <br /> later.

-17-

Failure to met the

TS action statement

was caused

by inadequate

corrective action for a previous similar occurrence.

During investigation of a similar failure on March 15,

1992,

the

licensee

determined that only the zero range

was affected

by the

failure,

and all the ranges

required for the indicator to fulfill

its safety function were operable.

The licensee

considers

previous

failures to be similarly of low safety significance.

In Inspection

Report 50-323/$ 2-01, the

NRC issued

a violation

concerning the inoperable

sump level indication.

This 'item is

closed.

Failure to Test

a Unit 2

ECCS Valve After Maintenance

LER 50-323

91-11

Revision

0

Closed

On October

17,

1991, while in Mode 5, the packing

on

ECCS valve

SI 2-8802B was adjusted

and the packing gland follower nuts were

torqued to a value greater

than the .torque

used for the last

successful

stroke time test.

Both these

operations result in

requirements

to perform a post-maintenance

test before returning the

valve to operable status.

However, neither requirement

was

immediately recognized.

During mode change

review on October 22,

the deficiency was recognized,

and the test

was performed.

As corrective action, training on mode transition

was provided for

the Engineering Test Group,

an Operations

event report was issued,

and work planning issued

enhanced

work policies.

Corrective action

for the generic

concern of personnel

errors will be addressed

by

Followup Item 50-275/91-27-02,

documented later in this report.

This item is therefore closed.

11.

0 en

a ~

Item Followu

92703

Public Address

PA

S stem

Powered

b

Non-Vital Circuitr

Followu

Item 50-275 91-09-03

Closed

b.

During the loss of offsite power event

on March 7,

1991, operators

were unable to quickly inform workers in the containment of plant

status

because

the

PA system

was powered from non-vital power.

Containment

was evacuated

in an orderly manner without use of the

PA

system.

The licensee

plans to implement control of PA system

power

sources

during outages.

Based

on planned licensee

actions, this

item is closed.

EDG Slow to Load

Followu

Item 50-275 91-09-04

C osed

This item discussed

the failure of EDG l-l to load onto the vital

bus within 10 seconds

during the loss of offsite power event

on

March 7,

1991.

After NRC review of the circumstances,

the licensee

received

a violation associated

with determination of the validity

of the start failure (50-275/91-07-10).

No other issues

were

identified.

Therefore, this item is closed.

0

18

Refuel in

Procedures

Chan

e

Foll owu

Item 50-275 91-09-05

Closed

During the loss of offsite power on March 7,

1991,

a concern

was

identified regarding the safety of fuel assembles

in transit during

a loss of offsite power.

The licensee identified a commitment

based

on

INPO SOER 85-01 to change

procedures

to include actions to place

fuel assemblies

in a safe, location during loss of refueling cavity

cooling concurrent with a loss of power.

The inspector reviewed Revision ll of procedure

OP B-BDS2, Core

Loading Sequence,

which was %evised to include

a step which does

not.

allow a fuel assembly to be lifted from the spent fuel pool until

the previous

assembly

has

been unlatched in the core.

The inspector verified that

a similar requirement

eMisted in the

core unloading procedure.

Based

on the licensee's

corrective

action, this item is closed.

Ino erable

Wide Ran

e Reactor Cavit

Sum

Followu

Item 50-323 92-

01-03

Closed

The

NRC issued

a Notice of Violation due to inoperable

wide range

reactor cavity sump level indication.

Since that time, the licensee

has successfully identified and corrected failure of the

sump level

indication

on two occasions,

as

a result of more attention to

Technical Specification operability requirements.

As permanent

corrective action,

continued troubleshooting

and repair work on the

level indication has occurred during unscheduled

outages.

A design

change

has

been reviewed for installation during the next scheduled

outage.

Based

on the licensee's

corrective actions to date,

and

planned corrective action, this item is closed.

Increase

in Personnel

Errors

Followu

Item 50-275 91-27-02

0

e

In addition to followup of existing licensee efforts to reduce the

number of personnel

errors, follow of corrective actions for this

item will include the generic corrective actions for licensee

event

reports

documented

above which were caused

by human error.

Indica-

tion of successful

actions will include reduction of the number of

LERs caused

by human error.

This item remains

open.

S urious Actuation of Carbon Dioxide Fire

Su

ressio

S stem in

EDG

1-3

Room

Unreso1ved

Item 50-275 92-05-01

Closed

During a routine monthly surveillance of the 1-3

EDG, the carbon

dioxide (cardox) suppression

system actuated.

The ventilation for

generator

cooling was then cut off as

a result of the cardox system

closing the west rolldown doors.

Operators

shut

down the diesel to

prevent overheating.

The

NRC questioned

whether this was

a valid

failure of the diesel.

Because

the root cause is still under

investigation,

and because

the licensee is reviewing the validity of

failure evaluations

in response

to an

NRC notice of violation, this

issue is closed.

Followup of the issue of validity of failure will

be part of routine resident

inspector activities.

-19-

g,

Com arison of Li uid Radwaste

Anal sis Results

Followu

Item

50-275 88-33-01

Closed

This item concerned

an inter-comparison of i-ron-55 (Fe-55) activity

in a liquid radwaste

sample that was split between

the licensee

and

the

NRC contract laboratory.

The initial inter-comparison of

analytical results for Fe-55 did not agree,

and

a followup

inspection

was conducted

at the licensee's'off-site

laboratory.

The

inspector found that the licensee's

laboratory sampling

and measure-

ment techniques

were fundamentally

sound.

To resolve the issue,

the

inspector,

in coordination with the licensee,

devised

an experiment

'o

independently verify both NRC's

and the licensee's

analytical

methods for determining

Fe-55 in liquid radwaste.

A liquid radwaste

sample,

spiked with FE-55,

was split between the

NRC contract

laboratory

and the licensee.

The amount of FE-55 activity was

known

only by the inspector.

Based

on the results of the inter-comparisons,

the inspector

concluded that the licensee's

method for analyzing liquid radwaste

for FE-55 is satisfactory.

This item is closed.

12.

Followu

on Unresolved

Items

92701

a ~

uxiliar Salt Water

ASW

Floodin

Due to Failure to Follow Proce-

dures

U

eso

ved Item 50-275

9 -24-01

C osed

On August 2,

1991, flooding of the component cooling water heat

exchanger

area occurred

as

a result of maintenance

worker s'ailure

to follow clearance

instructions in the order specified.

Review of

the safety significance of this issue determined that the other

trains of CCW and

ASW were available

and would have performed

their safety functions.

Licensee corrective actions

included issuing

a maintenance

event

summary,

counseling the individuals involved using positive

counseling,

and emphasizing

the personal

and plant safety aspects

of

properly following clearances.

The failure to follow clearance

instructions

appears

to be

a viola-

tion of Technical Specification 6.8. 1, which requires that work be

implemented

by procedures.

Based

on the licensee's

corrective

action

and the low safety significance of the concern,

the violation

is not being cited because

the criteria specified in Section V.A. of

the Enforcement Policy were satisfied

(92-16-05, closed).

Se aration of Safet

Related Electrical Circuits

Unresolved

Item

50-275 91-11-01

Closed

The licensee

had previously identified that two independent

Class

1E

direct current (dc) supplies

were electrically connected

in a non-

Class lE fire horn relay panel.

There

was

no electrical

separation

within the panel.

0

-20-

The licensee

concluded that connection of the two Class

1E dc

supplies in the relay panel

was within the separation criteria

established

by their license.

r

An inspector also previously noted that both Class

1E cables

and

non-Class

1E cables

were being routed through

a new Conax penetra-

tion.

The licensee

stated that they were using Regulatory Guide (RG) 1.75,

"Physical

Independence

of Elect'rical Systems,"

when

feasible during design modifications.

The licensee

stated that they

were using coax cables, for phich there were

no spare penetrations.

Therefore,

the licensee

concluded that separation

per

RG 1.75 was

not feasible.

The inspector determined that the routing of both Class

lE cables

.

and non-Class

1E cables

through the

new Conax penetration

would be

further reviewed for acceptable electrical separation.

The review

would be performed in conjunction with the review of the accepta-

bility of electrical separation within the fire horn relay panel.

The inspector evaluated

both of the previously identified items

discussed

above.

The inspector noted that the Diablo Canyon design

predated

RG 1.75.

The'esign

basis for Diablo Canyon included

IEEE 308-1971, "Criteria for Class

lE Electrical

Systems

for Nuclear

Power Stations."

Paragraph

5.3.5 of IEEE 308-1971 stated that

protective devices shall

be provided to isolate failed equipment

automatically.

The inspector reviewed the circuit design

and

concluded that the Diablo Canyon design for protective devices

was

adequate

to prevent faults in non-lE Class

panels

from affecting

Class

1E dc supplies.

The inspector also concluded that the installation of both Class

1E

and non-Class

1E cables in a new Conax penetration

met the design

criteria for Diablo Canyon.

The inspector

concluded that lack of a

spare penetration

was

a reasonable

evaluation for concluding that

installing the

new cables

per

RG 1.75 criteria was not feasible.

This item is closed.

4 Kilovolt Switch ear Fault Current Ratin

Unresolved

Item 50-275

and 50-323 91-07-01

Closed

The Electrical Distribution System Functional

Inspection identified

that calculated fault current exceeded

4 kilovolt (kV) switchgear

ratings during certain plant operations.

Calculated fault current

exceeded

switchgear ratings

when one or more emergency diesel

generators

(EDGs) were operated

in parallel with the main generator.

The licensee

took action to minimize the tests

which required para-

llel operation of the main generator

and one or more

EDGs.

The

licensee

also took action to minimize the fault capability of the

main generator

during parallel operation with an

EDG.

-21-

The licensee

performed

a calculation which showed that

a maximum

(bolted) fault was

a low probability event during the limited time

the main generator

was operated

in parallel with an

EDG.

The

NRC staff calculated the core

damage

frequency

caused

by the

occurrence of a bolted fault during

a time when the main generator

was operated

in parallel with an

EDG.

The calculation

showed that

the core

damage

frequency

caused

by this bolted fault was in the

order of 1.0E-9 per reactor year or less.

The inspector reviewed the 1'Icensee's

actions

and concluded that

these actions to minimize the risk from a bolted fault were

adequate.

The inspector reviewed the licensee's

calculation

and

concluded that this calculation

was adequate

to demonstrate

that

a

bolted fault during parallel operation of the main generator

and

an

EDG was

a low probability event.

The inspector also concluded that

the core

damage

frequency calculation demonstrated

that the bolted

fault condition discussed

above

had little safety significance.

This item is closed.

13.

Verification of As-Built Drawin s

37051

and

50073

On April 24-25,

1992, the inspector entered

containment to examine

containment

fan cooler damper 2-4 to verify the licensee

had restored

this component to the requirements of the design drawings

and documents.

The inspector

used the following documents

as the basis of this

inspection.

~

American Warming 5 Ventilating, Inc., Drawings SHW-D-9098,

PGKE

Revision 6, record 663079,

Sheet

37;

SHW-D-9099, Revision

B; and

81010-001-000

Revision A,

PGKE record 663079,

Sheet

75

~

Design

Change Notice DC2-EH-44664,

CFCU Backdraft Damper Helper

Springs

~

Non-Conformance

Report DC0-92-HH-N007, Containment

Fan Coolers

The inspector

observed that the backdraft

damper

appeared

to conform to

the design

documents with two exceptions.

First, several of the Allen

head shoulder bolts holding the horizontal linkage

arm to the individual

vane linkage

arms

appeared

loose in the holes in the linkage arms.

Second,

about half of the counterweights

on the ends of the linkage arms

did not contact the rubber block shock absorbers

when the damper

was

closed.

The gap

was 1/16 inch or less.

The design

documents

did not

specify any clearances

related to these observations.

When questioned

by the inspector,

the Hechanical

Maintenance

Engineer

showed the inspector

an Action Request

which had

been written regarding

the loose fit of the shoulder bolts in the linkage arms.

The licensee

concluded that this deficiency would not have prevented

the damper from

working and planned to completely overhaul

these

dampers

during the next

refueling outage.

-22-

The inspector re-entered

containment to observe the surveillance testing

(M-51A) of damper 2-4 to determine if the lack of contact with the shock

absorber

block would affect the operability of the damper.

The inspector

observed that starting

and stopping the associated

containment

fan cooler

unit caused

the damper to swing open

and .shut over

a period of several

seconds.

The inspector concluded that during normal operation the damper

would not be significantly affected

by the counterweights

not resting

on

the shock absorber

block.

The inspector requested

that 'the licensee

evaluate

the effect of the observed

gap

on the post-LOCA performance of

the dampers.

The licensee

evaluated

the observation

and concl'uded that during

a

LOCA,

with the gaps

measured

by the licensee,

the flexibilityof the linkage

mechanism

and the dampers

was sufficient so that the shock absorbers

would absorb

any significant shock to the linkage arms.

'o

violations or deviations

were identified.

14.

nformation Meetin

with Local Officials

94600

On May 4,

1992, the resident

inspectors

met with the

San Luis Obispo

County Administrator, Deputy Administrator,

and

Emergency

Response

Coordinator.

The purpose of the meeting

was to introduce the

NRC

inspectors,

to offer the NRC's openness

to discuss

inspection report

findings with the County,

and to discuss

general

issues of emergency

~

~

~

~

~

planning.

15.

~Fit

M

An exit meeting

was conducted

on June

12,

1992, with the licensee repre-

sentatives

identified in Paragraph

1.

The inspectors

summarized

the

scope

and findings of the inspection

as described

in this report.