ML16341F188

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Insp Repts 50-275/89-09 & 50-323/89-09 on 890305-0422 & 0505.No Violations or Deviations Noted.Major Areas Inspected:Plant Operations,Maint & Surveillance Activities, Followup of Onsite Events,Open Items & LERs
ML16341F188
Person / Time
Site: Diablo Canyon  Pacific Gas & Electric icon.png
Issue date: 05/16/1989
From: Mendonca M
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML16341F189 List:
References
50-275-89-09, 50-275-89-9, 50-323-89-09, 50-323-89-9, NUDOCS 8906050279
Download: ML16341F188 (38)


See also: IR 05000275/1989009

Text

U.

S.

NUCLEAR REGULATORY COMMISSION

REgION

V

Report Nos:

50-275/89-09

and 50-323/89-09

Docket Nos:

50-275

and 50-323

License

Nos:

DPR-80 and

DPR-82

Licensee:

Pacific Gas

and Electric Company

77 Beale Street,

Room 1451

San Francisco,

California 94106

Facility Name:

Diablo Canyon Units 1 and

2

Inspection at:

Diablo Canyon Site,

San Luis Obispo County, California

Inspection

Conducted:

March 5,

1989 through April 22 and

May 5,

1989

Inspectors:

P.

P. Narbut, Senior Resident Inspector

Approved by:

K.

E. Johnston,

Resident

Inspector

M.

M. Mendonca,

Chief

Reactor Projects

Section

1

~r ~Ye

Date Signed

~Summar:

Ins ection from March

5 throu

h

A ril 22 and

Ma

5

1989

Re ort Nos.

50-275/89-09

and 50-323/89-09

Areas Ins ected:

The inspection included routine inspections

of plant

operations,.

maintenance

and surveillance activities, follow-up of on-site

events,

open items,

and licensee

event reports

(LERs),

as well as selected

independent

inspection activities.

Inspection

Procedures

30703,

37702,

40500,

61726,

62703,

71707,

71710,

90712,

92700,

92701,

92702,

92720,

93702,

and

94703 were used

as guidance during this inspection.

Results of Ins ection:

No violations or deviations

were identified.

Areas of Stren ths

During the reporting period, the following strengths

were noted:

o

The licensee

has

expanded

the use of "Justification for Continued

Operation"

(JCO) evaluations.

The JCOs,

which were performed

on 10 CFR Part 21 issues,

the steam generator

tube plug issue,

and the leaking Unit

2 pressurizer

safety relief valve, indicate

a licensee

trend towards

06050278

890515

DR

ADOCK 09500

l2575

6

timely performance

analysis of plant and industry problems

as they apply

to the operational

safety of the Units.

o

It was noted that the licensee's

decision to shutdown to repair the

leaking Unit 2 pressurizer

safety relief valve was

a conservative

decision

made in the interest of safety.

The Technical Specifications

did not require

shutdown

and industry experience

was available to

indicate that the valve may have continued to be functional with greater

leak rates.

o

The licensee initiated a quarterly System Status

Report Program,

in which

the system engineer

and design engineer

review existing problems,

perform

a system walkdown,

and summarize planning

and proposed actions in a

report for management's

review.

Although the program is in its formative

stages, it appears

that the program will be

a good vehicle to strengthen

engineering

involvement in plant activities

and problems.

Areas of Weakness

During the reporting period weaknesses

were noted

as follows:

o

Continued instances

of equipment misalignment were noted.

Specific

examples

were the plant vent radiation monitor misalignment (section 4h)

and the racked out circulating water

pump potential

transformers

(section

41). It should

be noted that subsequent

to this report period,

on April

25, 1989, during an enforcement

conference

(see

Inspection

Report

50-275/89-15),

the licensee

proposed

extensive revisions to their

equipment lineup program to address

this problem area.

o

The licensee's

program for lubrication of important manual

valves

was

found to be not fully implemented despite

the fact that the issue

had

received

management

attention

subsequent

to a team inspection in February

1987.

The failure of the licensee

to ensure that such

commitments

are

successfully

completed in a timely and thorough manner

was

a subject of

the enforcement

conference

of April 25,

1989 (Inspection

Report

50-275/89-15).

DETAILS

Persons

Contacted

J;

D. Townsend,

Plant Manager

"D. B. Miklush, Assistant Plant Manager,

Maintenance

Services

"L'. F.

Womack, Assistant Plant Manager,

Operations

Services

B.

W. Giffin, Assistant Plant Manager,

Technical

Services

"C.

L. Eldridge, Quality Control Manager

"W. T.

Rapp, Onsite Safety

Review Group Chairman

T.

A. Bennett,

Maintenance

Manager

"D. A. Taggert, Director Quality Support

"B.

D. Guilbeault, Material Services

Manager

W.

G. Crockett,

Instrumentation

and Control Maintenance

Manager

J.

V. Boots,

Chemistry

and Radiation Protection

Manager

"T.

L. Grebel,

Regulatory Compliance Supervisor

"M. J.

Angus,

Work Planning

Manager

"J.

A. Shoulders,

Onsite Project Engineering

Group Manager

"M.

E.

Leppke,

Engineering

Manager

S.

R. Fridley, Operations

Manager

R.

P.

Powers,

Radiation Protection

Manager

M.

R. Tresler,

Project Engineer

E.

C. Connell, Assistant Project Engineer

The inspectors

interviewed several

other licensee

employees

including

shift foremen

(SFM), reactor

and auxiliary operators,

maintenance

personnel,

plant technicians

and engineers,

quality assurance

personnel

and general

construction/startup

personnel.

Denotes

those attending the exit interview on May 5, 1989.

The exit

meeting

was delayed

from the week of April 22 due to the involvement

of plant management

and the inspectors

in preparations

for the

enforcement

conference

held on April 25,

1989.

0 erational

Status of Diablo Can

on Units 1 and

2

During the inspection period both units remained at 100K power except for

periodic condenser

cleaning

and an Unit 2 outage,

beginning April 7 and

continuing to April 15, to replace

a leaking pressurizer

code safety

relief valve.

Unit 2 experienced

an avoidable reactor trip on April 16,"

1989, at 50K power during power ascension

following the outage.

A load

rejection occurred

due to the opening of the units output breakers.

The

reactor did not operate

through the load rejection

as designed

due to the

loss of the ocean circulating water system

due to an electrical

equipment

lineup error.

Unit 1 operated at power throughout the inspection period.

3.

0 erational

Safet

Verification

71707

a ~

General

During the inspection period, the inspectors

observed

and examined

activities to verify the operational

safety of the licensee's

facility.

The observations

and examinations

of those activities

were conducted

on a daily, weekly or monthly basis.

On a daily basis,

the inspectors

observed control

room activities to

verify compliance with selected

Limiting Conditions for Operations

(LCOs) as prescribed

in the facility Technical Specifications

(TS).

Logs, instrumentation,

recorder

traces,

and other operational

records

were examined to obtain information on plant conditions,

and

trends

were reviewed for compliance with regulatory requirements.

Shift turnovers

were observed

on a sample basis to verify that all

pertinent information of plant status

was relayed.

During each

week, the inspectors

toured the accessible

areas

of the facility to

observe

the following:

(a)

General plant and equipment conditions.

(b)

Fire hazards

and fire fighting equipment.

(c)

Radiation protection controls.

(d)

Conduct of selected activities for compliance with the

licensee's

administrative controls

and approved procedures.

(e)

Interiors of electrical

and control panels.

(f)

Implementation of selected

portions of the licensee's

physical

security plan.

(g)

Plant housekeeping

and cleanliness.

(h)

Engineered safety feature

equipment alignment

and conditions.

(i)

Storage of pressurized

gas bottles.

The inspectors

talked with operators

in the control

room,

and other

plant personnel.

The discussions

centered

on pertinent topics of

general

plant conditions,

procedures,

security, training,

and other

aspects

of the involved work activities.

I

No violations or deviations

were identified.

4.

Onsite Event Follow-u

93702

a 0

Im ro er Control of Radio ra

h

On March 6, 1989, the licensee notified the residents

of problems

incurred by a radiography contractor

performing nondestructiVe

examination in the turbine building.

The contractor

had failed to

perform adequate

postings,

barriers,

and surveys.

These conditions

were found by the licensee's

health physics personnel

and the job

was stopped.

The licensee

concluded

no overexposures

were involved.

The highest exposure

was estimated

to be four mi llirem.

A

nonconformance

was written.

The regional inspection staff notified

the licensing authority for the radiographer

and action

was taken

by that authority.,

Auxiliar Buildin Ventilation Fan Fails to Start

Due to a

Maintenance

Error

On March 8, 1989,

mechanical

maintenance

personnel

reported off a

clearance

on Auxiliary Building Ventilation Fan S-33,

signed the

shift foreman's

Technical Specifications

sheet reporting that the

fan was operable

and indicated that

no work had been performed

on

Fan Discharge

Damper M-21 as scheduled.

Later that day,

when

operations

attempted to start

Fan S-33,

the fan failed to run

because

Fan Discharge

Damper M-21 failed to open.

It was later

discovered that the actuator for damper

M-21 had been in fact

partially disassembled

by the maintenance

mechanic.

The confusion

appeared

to stem from the mechanic's failure to document his actions

(which were beyond those stated

in the work order)

and poor verbal

turnover from the mechanic to his foreman

and that foreman to his

relief.

The licensee initiated a guality Evaluation

and an

evaluation in accordance

with the

Human Performance

Evaluation

System

(HPES).

The

HPES evaluation

had not been completed at the

end of the report period.

Licensee corrective action will be

followed up during routine inspection.

Ten Percent

Atmos heric Steam

Dum s 0 en At Power

On March 13, 1989, the Unit 2 10K steam

dump valves

opened

unexpectedly

when

a main turbine first stage

pressure

channel

(PT

506) was

removed from service for calibration.

The licensee

determined that the actuation resulted

from an out of

calibration module which inputs to steam

dump demand logic.

Further, it was determined that the module was out of calibration

because

contract technicians,

while attempting to calibrate

another

module,

had inadvertently adjusted

the wrong module.

The licensee

determined the root cause to be personnel

error with

the technicians failing to perform adequate self-verification.

Corrective actions

focused

on emphasizing

the self-verification

policy and to revise existing policy,to allow only experienced

technicians

to work independently in the "Hagan" racks,

which

contain plant controls instrumentation.

The inspector

has reviewed

the licensee's

actions

and found them acceptable.

Unit 1 Containment Ventilation Isolation

On March 14, 1989, Unit 1 experienced

a containment ventilation

isolation (CVI) due to an I8C technician working on leads to the

ESF

Equipment

Rooms temperature

monitor annunciator

alarm.

The

technician inadvertently grounded the power lead with a screwdriver.

This resulted in a voltage transient

on a vital instrument inverter

which initiated the CVI.

The licensee

prepared

nonconformance

report

NCR DCI-89-TI N027 and event report LER-1-89-001.

Corrective actions described

in the

LER involve counseling the

technician regarding precautions

for working on energized

equipment,

training all I8C technicians

on the event,

and developing

a policy

to clear

power circuits whenever feasible

(as it was in this case).

The inspector

found these

actions acceptable.

Wron

Oil Used In Turbine Driven Auxiliar

Feedwater

Pum

s=

On March 18,

1989, the licensee

operations

personnel

discovered that

the wrong oil had been

used in Auxiliary Feedwater

Pump 2-1 when oil

in the turbine

had been

changed following testing.

The pump was declared

inoperable, its oil was changed

and it was

declared

operable

the next day after analysis,

testing

and

contacting the vendor.

The vendor

had stated that due to its

slightly higher viscosity, the oil used

may have resulted in

slightly higher bearing temperatures

but was not harmful.

On the

same

day of the event,

the licensee

launched

an investigation

first into the other auxiliary feedwater

pumps

and then into all

other safety related

pumps to determine if any other

pumps

had

received

improper oil.

The results of the investigation

showed that

Unit 1 auxiliary feedwater

pump l-l had also received the wrong oil.

Additionally, the investigation revealed that containment

spray

pump

2-2 was not in the recurring task work order program and

consequently

did not have its oil changed

every 18 months

and had

not had an oil change

since August 8, 1985.

The other containment

spray

pumps (l-l, 1-2,

and 2-1) had been properly handled.

The primary cause of the lubrication problems

were:

1) for the

auxiliary feedwater

pumps,

the recurring task work orders specified

the wrong oil contrary to the licensee's

lubrication schedule.

A

total of four incorrect work orders

were found involving three

separate

work planners;

and 2) for the containment

spray

pump motor,

the problem appeared

to stem from the conversion

(from one system to

another) of the computer tracking of recurring tasks.

The licensee

prepared

two nonconformances

on the problems,

NCR

DC2"89

WP N029 for the auxiliary feedwater

pumps

and

NCR DCO-89

WP

N030 for the containment

spray

pumps.

The licensee

s initial

actions

were sufficient to thoroughly examine for other lubrication

problems.

The licensee's

actions to prevent recurrence

did not

initially appear to require

independent verification of work order

accuracy.

The licensee's

actions in this regard were couched in

language

such

as "Research

the possibility of gC verification of

correctness

of oil types."

Initial discussions

with the Assistant Plant Manager for Maintenance

indicated that the verification of work. order accuracy

was intended

to be the responsibility of the job foreman.

He stated this

responsibility would be reemphasized

in a maintenance bulletin.

The

inspectors will follow-up the licensee's

actions regarding

verification activities in the work planning center

(Follow-up item

50-275/89-09-01).

Fire Water Valves not in Sealed

Valve Pro

ram

On March 20, 1989,

a licensee guality Assurance

audit identified two

valves that were not sealed to verify position as required

by

Technical Specifications (TS) 4.7.9. l.c.

The valves were fire

protection valves

FP-1-1294

and FP-2-1294.

The valves

wer e in their

required

open position.

The valves

had been

added to the fire

protection

system in December

1988 as part of a design

change .to

provide an alternate

source of cooling water to the charging

pump

seal

and oil coolers.

The licensee

prepared

a nonconformance

report (DCP-89-SS-N033)

and

an event report

(LER 1-89-003).

The details of the event

and the

licensee's

corrective action were reviewed

and determined to be

acceptable

by the inspector.

LER 1-89-003 is closed.

Leakin

Pressurizer

Code Safet

Valve and Resultin

Un lanned Outa

e

On March 21,

1989, Unit 2 Pressurizer

Code Safety Relief Valve 8010A

was identified to be leaking at approximately 0.2

gpm.

The valve

exhibited

an unexpected

leakage characteristic

in that the leakage

was not constant

and would periodically appear

in the form of relief

discharge line sonic and temperature

alarms.

The resultant

leakage

rate over

2 hour2.314815e-5 days <br />5.555556e-4 hours <br />3.306878e-6 weeks <br />7.61e-7 months <br /> periods

averaged

about 0.2

gpm.

Sonic alarms

were

received

over

a period of days.

Alarms were received

from as few as

2 per day to as

many as

12 per day.

The duration of the alarms

were

generally several

seconds

and in a few cases

minutes in duration,

the longest being

6 minutes

and ll seconds

on April 3,

1989.

The

leakage

was in some

cases

accompanied by'ressurizer relief tank

pressure

incr eases,

and in a few cases,

a pressurizer

pressure

decrease.

Operations with the leaking valve continued until April

8,

1989 when the unit was shut

down to replace

the valve.

The

shutdown

was precipitated

by increased

short duration leakage of up

to 3 gpm.

Between

March 21, 1989,

and the plant shutdown,

the licensee's

safety evaluation (justification for continued operations)

was based

on the following:

Technical Specification 3.4.6.2,

Reactor Coolant System

(RCS)

Leakage Limits, identified

RCS leakage to 10 gpm.

This limit

was based

in part on the ability of the charging

system to make

up the leakage.

Therefore,

the leakage

did not violate

technical specification limits.

Discussions

with other utilities indicated that the leakage

characteristic

experienced

at Diablo Canyon

was similar to that

experienced

at other sites.

In some cases,

other sites

had

operated for extended

periods of time.

h

5

IH

o

Discussions with other utilities and the vendor revealed that

this phenomena

had not resulted in valve failures

and did not

represent

a severely

degraded

valve.

o

The licensee

determined that leakage

past the seat of the valve

would not affect valve actuation if required to function.

The licensee

issued

a safety evaluation (justification for continued

operations)

on April 6, 1989.

During the week long outage,

the licensee

took Unit 2 to Mode 5

(cold shutdown),

removed the Pressurizer

Relief Valve 8010A and

replaced it with a spare

valve (originally, Unit 1 valve 8010B).

The licensee

found that the spare

valve had

a slightly larger inlet

flange (as cast)

and did not provide proper clearances

with the

seismic restraint installed for the-original valve.

The licensee

initiated a Design

Change

Package

(DCP) to provide the proper

clearances.

The inspector

reviewed the

DCP and witnessed portions

of the installation effort and found them acceptable.

The inspector also inquired to what extent pressurizer

relief valves

had been

"swapped"

and if it was possible

any had been inserted in

restraints with inadequately

clearance.

The maintenance

engineer

responsible

for pipe supports

and restraints

stated

the issue

had

been

reviewed

and that for Unit 1, the unit in operation at the

time, all valves

had been in place since original startup.

For the

Unit 1 valves,

hot functional tests

and,

on subsequent

startups,

walkdowns performed in conjunction with the snubber reduction

program provided assurance

that binding was not taking place.

In

addition,

none of the valves

had

shown any excessive

leakage

(a

possible result of binding).

Unit 2 valves

8010B and 8010C

had also

been in place since startup

and subject to hot functional testing.

The licensee

committed to revise the valve installation procedure

to

include steps to verify the gap between

the valve and the pipe

restraint.

The inspector

found these

proposed actions acceptable.

Plant Vent Radiation Monitor Ino erable

Due to Valve Misali nment

On March 27, 1989, operating personnel

discovered that one set of

the radiation monitors for monitoring the plant vent for noble gas

(RM-14A) and for particulate contamination

(RM-28A) was inoperable

due to a mispositioned switch.

The switch was in the "purge"

position rather

than the "sample" position causing the monitors to

sample air from the auxiliary building environment rather than from

the plant vent.

Licensee analysis

determined that the switch had been

most probably

mispositioned

by IKC personnel

on March 23, 1989,

subsequent

to

maintenance.

During the period of inoperability

a containment

purge

was conducted

on March 25,

1989.

However during this purge the

second set of pl.ant vent monitors

(RM-14B and

RM-28B) were operable,

as were the containment monitors (RM-ll and RM-12) which did not

indicate

a problem with the discharge.

The licensee

prepared

a nonconformance

report and an event report

LER 1-89-004 describing the event

and corrective actions.

The inspectors

reviewed the licensee corrective actions

and found

them to be acceptable.

The actions

included improvements

in

detailed verifications for the operating procedure

for containment

purging, the I8C procedure for returning the radiation monitoring

equipment to service

and, the operating procedure for swift

operability checks.

The licensee

actions also include the broader

action of revising all I8C procedures

to add specific item-by-item

steps

to be checked

and verified in returning equipment to service.

Not included in the

LER were broader actions

committed to in an

April 25,

1989,

enforcement

conference

(NRC report 50-275/89-15) in

which the licensee

committed to actions to improve personnel

accountability

and equipment lineup control.

LER 1-89-004 is considered

closed.

The activities discussed

in this section involved apparent

or

potential violation of NRC requirements

identified by the licensee

for which appropriate

licensee

actions

were taken or initiated.

Consistent with Section

V.A of the

NRC Enforcement Policy,

enforcement action was .not initiated by Region

V.

Containment Ventilation Isolation

Due to Failed Fuses

on Plant Vent

Radiation Monitor

On March 31, 1989, at 8: 52 a.m.,

fuses for Unit 2 instrument

power

supplying plant ventilation radiation monitor RM-28 blew,

deenergizing

the radiation monitor and initiating a Containment

Ventilation Isolation (CVI).

This event is described

in

LER

2-89-03,

issued April 28,

1989.

The licensee's

troubleshooting

and investigative activities were not

successful

in determining the root cause of the blown fuses.

There

have

been

no previous similar failures at Diablo Canyon,

and the

vendor (Westinghouse)

indicated that

no similar failures of

radiation monitor instrument power fuses

have

been reported.

The

subject fuses

have

been sent to a laboratory for analysis.

The inspector

reviewed the licensee's

troubleshooting

and

investigative activities and found them to be comprehensive.

LER

2"89"03 is closed.

I

Hi h Motor Stator

Tem eratures

Due to Hot Weather

On April 7, 1989, during a period of unusually hot weather at the

site the inspector

noted

a number of vital and

non vital pump motors

were alarmed

due to high stator

temperature.

The inspector

questioned

operators

as to what their procedures

required

them to do

and at what point they would question operability.

The results of

the conversations

were that the operators

had previous experience

with hot weather,

knew the alarm setpoints

were about

230 degrees

F

and considered

the situation unavoidable

but were alert to check

and

trend for temperatures

in excess

of those previously experienced.

The inspector discussed

the situation with operations

management

who

committed to have operability limits defined

and incorporated in

annunciator

response

procedures.

Maintenance

engineering

personnel

subsequently

provided. information which indicated that motor

manufacturers

consider the motors in question rated for 40 year life

with stator temperatures

of 248 degrees

F of less.

The inspector also questioned

the

gC manager

as to what degree

the

gC personnel

involved in operations

were instructed to look for such

situations

and elevate

them to attention.

The

gC manager

explained

that

gC could surface

such questions

and raise

them to management

attention through several

means.

The licensee's

actions

regarding this matter appeared

to be

acceptable

with the exception of a lack of aggressive

problem

identification on the part of operations

and

gC in recognizing the

absence

of pertinent temperature limit information from engineering

personnel.

This will be followed on routine inspection.

Feedwater Isolation

ESF

Due to Hi Steam Generator

Level

On April 8, 1989, at 1:39 p.m., while Unit 2 was in Mode

3 (Hot

Standby) in the process .of a cooldown to cold shutdown for repairs

on the leaking pressurizer

safety valve,

Steam Generator

2-4 water

level exceeded its high-high level setpoint, initiating feedwater

isolation and turbine trip signals.

The high-high level resulted

from Loop 4 main feedwater isolation valve testing.

Prior to the

test,

which is required

on a shutdown frequency,

the operators

verified that the main feedwater regulating

and bypass

valves were

closed.

However,

when the upstream

main feedwater isolation valve

was

opened for testing

steam generator

level increased.

Since the

valve must fully open prior to closure,

and full cycle takes

approximately

2 minutes,

steam generator

level increased

to its

high-high level setpoint before the valve could be closed.

The

inspector verified selected

portions of this event.

The licensee

will issue

an

LER describing the event.

The cause

and corrective

actions

discussed

in the

LER will be reviewed in a future inspection.

Unit 2 Reactor Tri

Followin

Generator

Loss of Load

On April 16,

1989 at 8:05 p.m., following the unexpected

opening of

the Unit 2 generator

output breakers,

a reactor trip resulted

from

low steam generator

level.

All safety

systems

responded

to the

reactor trip as designed.

However, the reactor trip was not

expected

since the plant is designed

to withstand

a 50K load

rejection without a reactor trip by the use of steam

dumps'.

Event Oescri tion

At 8:05 p.m., the generator

output breakers

(PCBs

542 and 642)

opened

as

a result of the actuation of Generator

Backup Relay 21G2.

'elay

21G2 is

a slow acting backup

system

designed to detect faults

from the generator

output through the transmission

lines.

At the

same time,

a transfer

from auxiliary power (normal alignment from

the main generator)

to startup

power was initiated by Generator

Undervoltage

Relay 27G2.

In the transfer to startup

power, the

Circulating Water

Pump

(CWP) selected for auto transfer did not load

onto the star tup bus.

The loss of the

CWP disabled the condenser'steam

dumps.

The opening

of the output breakers

resulted in a loss of load to the turbine.

Without the condenser

steam

dumps,

steam line pressure

and

RCS

pressure

elevated to.the

lOX atmospheric

steam

dump set point of

1035 psi

and the pressurizer

power operated relief valve

(PORV)

setpoint of 2335 psi, respectively,

actuating

both sets of valves.

In addition, the reduced

steam flow caused

steam generator

level to

shrink.

Fourteen

seconds

following the opening of the output

breakers,

the reactor tripped on low steam generator level.

The

system

behaved

as designed, given the loss of condenser

steam

dumps.

All safety

systems

responded

as designed.

Following the event there were three

areas

not understood

by the

licensee:

o

The cause of the actuation of Generator

Backup Relay 21G2.

o

The cause of the actuation of Generator

Undervoltage

Relay

27G2.

o

The cause of the

CWP failing to load onto the startup

bus.

Other minor problems experienced

following the event included:

o

15 minutes following the trip, the unit differential current

annunciator

began to "chatter"

and created

a nuisance

alarm.

The differential current relay had not actuated

and there

was

no current in the system

when the annunciator

actuated.

o

The backup event recording

system did not actuate

and save data

as designed.

Likewise a temporary annunciator

alarm typewriter

did not function.

o

Reactor

Coolant

Pump 2-4 indicated excessive

vibration

following the event.

The licensee initiated an Event Investigation

Team (EIT) in

accordance

with plant procedures

on the morning following the event.

Generator

Backu

and Undervolta

e Rela

Actuations

The licensee

was unable to determine

the cause of the actuation of

Relays'1G2

and

27G2.

The investigation

focused

on all potential

causes

for the actuation including:

10

o

An inspection of the motor operated

disconnects

on the

generator;

o

An inspection of transmission

lines to the substation;

o

Bench testing

and subsequent

functional testing of relays

21G2,

27G2,

and time delay relay 62G2;

o

Continuity testing from the potential transformers

(PTs) which

supply generator voltages.to

the relays.

This included

turn-to-turn measurements

on the primary and secondary

sides of

the

PTs.

While the licensee's

investigation did not identify any

abnormalities, it was determined that

a momentary loss of the

B

phase

PT voltage would initiate the sequence

of events

as

experienced.

Prior to plant startup

on April 19 the licensee

instrumented all phases

of the

PT in question

and Relay 21G2.

The

inspectors

concluded this plan was acceptable.

~CWP Tri

On the transfer

from auxiliary to star tup power initiated by relay

27G2, the breaker for the

CWP 2-1 motor, which was selected for auto

transfer,

should

have tripped and then re-closed

when motor voltage

had. adequately

decayed.

The breaker tripped, but failed to

re-close.

On inspection of the breaker it was found that the

breaker

PT drawer

had been racked out.

This occurred

because

of

equipment lineup problems during the one week outage to repair

a

leaking pressurizer

code safety valve.

The

CWP breaker

PT provides motor voltages to the motor undervoltage

relay.

The relay is a permissive in the breaker

auto transfer logic

that will not allow the breaker to close until the motor voltage

has

decayed to 25K.

With the

PT drawer racked out, the undervoltage

permissive

was active

so that without any time delay following the

trip signal, the breaker received

a close signal.

The breaker's

anti-pumping relay, which actuates

when the breaker receives

conflicting instructions,

actuated to keep the breaker tripped.

This explanation

was subsequently

verified by testing.

The

PT drawer

was

opened during the seven

day pressurizer relief

valve maintenance

outage

and not reclosed prior to the restart of

the

CWP.

The

CWP motor breaker

had been cleared for cleaning of the

circulatinq water tunnels.

The clearance

request

issued for the

cleaning required the clearing of the

CWP motor breaker.

The

clearance

procedure

(NPAP C-6 Revision 6) required that

a switching

log be used

when clearing electrical

equipment.

Switching of 12kV

breakers

was controlled by operations" procedure

OP J-5: IV Revision

5, "Operating Procedure

12

KV Breaker

Code Order," which included

generic switching logs for 12kV breakers.

Step

Number

9 of the

removal

from service switching log states

for the

PT drawers

"Rack"out and hang

MOL LMan On Linej tag (if applicable)."

Although the clearance

request did not include

a step to rack out

the

PT drawer, operating procedure

OP E-4: III, "Circulating Mater

System - Shutdown

and Clearing" required that the

PTs

be racked out

when clearing the motor.

The operator filling out the switching log crossed

out "hang

MOL tag

(if applicable)"

and racked out the

PT drawer.

Three

days later,

another operator

returning the motor to service,

using

a return to

service switching log and the clearance

request,

marked the step to

rack the

PT drawer in as "N/A" and did not rack in the breaker.

The

PT drawer is located in back of the breaker cubicle.

Since the

PT

drawer only inputs to the auto transfer logic, the

pump was able to

startup.

The inspector identified the following weaknesses;

o

The procedures

applicable to the switching of electrical

equipment conflicted and

as

a result were not adequate

to

ensure that the task was accomplished correctly.

1)

The return to service switching log did not require the

use of the remove from service switching log as

a

reference.

2)

The procedure did not reference

switching procedure

OP

J-5: IV to require the use of the switching log.

3)

The clearance

procedure

NPAP C-6 required the use. of the

switching log, but did not specify

how the two are to

interface.

~

o

The operator

removing the breaker

from service did not modify

the clearance

to indicate that the

PT drawer was racked out.

o

The operator

returning the breaker to service did not verify

that the

PT was not racked out prior to marking the step to

rack it in "N/A."

The inspector discussed

these findings with the Assistant Plant

Manager for Operation

who agreed with the findings and stated that

corrective actions

such

as breaker specific switching logs, revised

procedures,

and operator training had been initiated.

Equipment lineup errors,

such

as this,

have

been

an issue in

previous reports (Inspection Reports

89-05 and 89-13)

and the

subject of the Enforcement

Conference

on April 25,

1989 (Inspection

Report 89-15).

In this instance,

procedures

for equipment lineup

were not adequate

to ensure that switching was satisfactorily

accomplished.

As a result, following a load rejection which the

plant was designed to accommodate

without a reactor trip, the

reactor

nonetheless

tripped and unnecessarily

challenged

safety

systems.

This is an apparent violation identified by the licensee

for which appropriate

licensee

actions

were initiated.

Consistent

with Section

V.A of the 10 CFR Part 2, Appendix C, enforcement

discretion

was exercised

by Region

V.

The corrective actions

12

discussed

in the April 25,

1989 meeting will be the subject of

follow-up inspection.

Wron

Sized Part

Used

on Fan Motors

On April 19, 1989, the licensee

became

aware of a problem with

replacement

parts

used

on Auxiliary Building Fan S-32.

The fan is

belt driven by an electric motor.

The motors belt sheave

had been

replaced,

due to wear,

on April ll and was declared

operable

on

April 14,

1989.

The belt sheave

was oversize

and resulted in higher

fan speed

and greater

motor current draw.

The problem was

discovered

on April 17, 1989, duringdelayed post maintenance

testing

and

came to managements

attention

on April 19,

1989.

The occurrence

involved several

weaknesses

and errors in the

execution of the licensee's

maintenance

program

and parts dedication

program.

The wrong part was installed

due to poor understanding

of

part number meaning,

improper tagging of the part,

mechanics

improperly verifying size,

and poorly laid out work orders which did

not require the acquisition of fan operating data before declaration

of operability.

Licensee

management

recognized

the seriousness

of the error and the

multiple mistakes

made.

They investigated

the effects ot the

mistake including breaker settings,

diesel

fuel oil consumption,

diesel

loadings, air flow disturbances,

and fan and motor effects.

Overall, the licensee. concluded that the involved systems

were not

impaired.

The licensee

prepared

a nonconformance

report on the problem.

The

inspectors will follow-up the licensee's

actions to prevent

recurrence.

10 CFR 50.59 Evaluations

Justifications for Continued

0 eration

a.

NPS Industries

10 CFR Part 21 Notification Re ardin

Potentiall

Defective Struts

and Snubbers

On March 7, 1989,

NPS Industries transmitted

a 10 CFR Part 21

notification to the licensee

advising that certain

model struts

and

snubbers

were potentially defective.

The licensee

had purchased

255

of the potentially defective struts

and

no effected snubbers.

The licensee

designed piping systems

such that given the combination

of all potential

movement,

including thermal

and seismic

movement,

struts

and snubbers

would be required to swing less

than

a five

degree

angle.

Their acceptance

criteria on the installation of

'truts

and snubbers

has

been that they accommodate

a greater

than

five degree

swing.

In summary,

the

NPS

10 CFR Part 21 report stated

that, given the combination of unfavorable tolerances,

certain

struts'ould

have

a less

than five degree

swing angle.

13

The licensee

performed

a 10.CFR 50.59 evaluation (Justification For

Continued Operation).

In summary,

continued operation

was based

on

the following:

o

The safety evaluation

by NPSI, which in essence

states that

a

strut will still accept rated load following deformation except

in situations

where repeated yielding could occur.

o

~

Initial hot functional

and post refueling walkdowns

have not

indicated failures of a nature described in the vendor's

10 CFR Part 21 analysis.

o

A walk down of all accessible

struts with potential for

inadequate

swing allowances will be performed prior to the next

refueling outages.

By the completion of the next refueling

outages,

all affected struts will have

been identified and

corrected.

The inspector

found this evaluation

and corrective action

acceptable.

b.

Steam Generator

Tube Plu

s

On January

17, 1989, Westinghouse

informed several

licensees

that

a

few utilities had observed dripping or wetness

around tube ends

plugged with Westinghouse

mechanical

plugs

and that upon further

examination

the plugs were failing due to inter-granular

stress

corrosion cracking

(IGSCC).

Westinghouse

further identified two

heats of plugs which appeared

to be susceptible

to

IGSCC due to

inadequate

heat treating.

Subsequently,

North Anna Unit 1

experienced

a failure of a steam generator

tube plug which had been

identified as susceptible

to IGSCC.

The failed plug was forced

through the dry steam generator

tube

and punctured the tube at the

U-bend, resulting in a 70

gpm primary to secondary

leak.

Westinghouse

notified Diablo Canyon of 23 steam generator

tube plugs

installed in Unit 2 from the affected heats.

In response

to this

notification and

NRC Information Notice 89-33,

on April ll, 1988,

the licensee

performed

a 50.59 evaluation.

In summary,

the licensee

based its evaluation

on the following

factors;

o

19 of the 23 tube plugs were "sentinel" plugs installed in the

1988 refueling outage.

These plugs,

which are only installed

in tubes that have not developed

leakage,

are designed with a

small

opening in the plug to serve

as

a warning if the tube

subsequently fails't was determined

by the licensee

and

Westinghouse

that since these

tubes plugs

have water

on both

sides of the tube plug,

a broken tube plug could not establish

enough force to rupture the tube wall.

o

Of the remaining four tubes plugs, all of which were installed

in 1987,

two were located in a tube with a small hole.

As a

0

14

result the tube was completely filled and, similar to the

sentinel

plugs, the plugs would not be capable of acquiring the

force to rupture

a tube.

o

It was determined that two remaining plugs in one dry tube

could potentially fail and cause

a tube rupture.

o

The North Anna hot leg temperature

is 618 degrees

F whereas

the

Diablo Canyon hot leg temperature

is 606 degrees

'F.

Since the

rate of IGSCC is temperature

dependent,

this provides

some

degree of margin.

o

Westinghouse

determined that primary to secondary

leakage

would

be limited to 77

gpm since flow would be restricted

by the

intact portion of the plug.

In addition, it was determined

that the propelled portion of the plug, after exiting the tube,

would not have

enough

energy to rupture

a second

tube.

o

The plant design basis

assumes

a much larger steam generator

tube rupture than

77

gpm.

Plant design

and emergency

operating

procedures

are based

on primary to secondary

leaks

much greater

than this.

The licensee

determined that based

o'n the above, Unit 2 could safely

operate to its next refueling outage at the beginning of 1990.

Long

t'erm corrective actions

had not been identified at the time of this

report, but were to be the subject of generic discussions

between

Westinghouse,

the

NRC, and all affected licensees.

The inspector

found the licensee's

evaluation acceptable.

No violations or deviations

were identified.

6.

Maintenance

62703

a o

Maintenance Activit Observation

The inspectors

observed portions of, and reviewed records

on, the

following maintenance activities to assure

compliance with approved

procedures,

Technical Specifications,

and appropriate

industry codes

and standards.

Furthermore,

the inspectors verified maintenance

activities were performed

by qualified personnel,

in accordance

with

fire protection

and housekeeping

controls,

and replacement

parts

were appropriately certified.

o

Diesel generator air start motor air regulator

replacement

o

Leak repair of Main Steam

Line Drain Valve MS-2-909

o

10K Steam

Dump Valve PCV-2-22 positioner adjustment

o

Centrifugal Charging

Pump 1-1 lube oil pump removal

o

Unit 2 pressurizer

code safety valve 8010A replacement.

15

b.

Maintenance of Manual Valves Called

On In Emer

enc

and Abnormal

Procedures

An NRC team inspection,

conducted

in February

1987 (Inspection

Report 87-01) identified that the licensee

did not have

a

maintenance

program for manual

valves.

During the inspection,

the

licensee

stated that the development of a program was

underway

and

it would address

the maintenance

of manual

valves that need to be

operated

during accident

and recovery periods.

In a June

15,

1987.

letter, the licensee

stated that Operations

would implement

a manual

valve exercising

and lubrication program for manual

valves that

may

be needed for the mitigation of significant transient

events.

The licensee

completed this commitment in June

1988,

by adding steps

to the sealed

valve verification procedure requiring all sealed

valves to be lubricated

and stroked.

One of the discrepancies

identified by Engineering in the

development of a design basis

document for the Auxiliary Feedwater

system

was that the cross"tie valves

between outlets of the two

motor driven pumps,

which are cal.led

upon in emergency

procedures,

were not in any maintenance

program.

The inspector discussed

this

finding with the Operations

Manager,

noting that there potentially

was

a large

number of valves

needed for "the mitigation of

significant transient events,"

which were not in, the sealed

valve

program.

The Operations

Manager concurred

and committed to have

a

comprehensive

review of emergency

and abnormal

procedures

to

identify those valves not covered

by the sealed

valve program.

Although the

new commitment is acceptable,

this is the action which

the inspector

expected

to have

been conducted initially.

While the

addition of a step to the sealed

valve program

was

a quick and easy

initial step, it is readily apparent that it alone did not fully

address

the commitment.

No violations or deviations

were identified.

Sur vei 1 lance

61726

By direct observation

and record review of selected

surveillance testing,

the inspectors

assured

compliance with TS requirements

and plant

procedures.

The inspectors verified that test equipment

was calibrated,

and acceptance

criteria were met or appropriately dispositioned.

The

inspectors

observed

selected

portions of Surveillance Test Procedure I-lA

and found it acceptable.

No violations or deviations

wer e identified.

En ineerin

Safet

Feature Verification

71710

The inspector walked

down the Unit 1 high head

and intermediate

head

safety injection systems

in accordance

with Inspection

Procedure

71710.

No findings were identified.

No violations or deviations

were identified.

9.

Radi ol o ical Protecti on

71707

'l

The inspectors periodically observed radiological protection practices to

determine whether the licensee's

program was being implemented in

conformance with facility policies

and procedures

and in compliance with

regulatory requirements.

The inspectors verified that health physics

supervisors

and professionals

conducted frequent plant tours to observe

activities in progress

and were generally

aware of significant plant

activities, particularly those related to radiological conditions and/or

challenges.

ALARA consideration

was found to be an integral part of each

radiation work permit.

No violations or deviations

were identified.

10.

Ph sical Securit

71707

Security activities were observed for conformance with regulatory

requirements,

implementation of the site security plan,

and

administrative procedures

including vehicle and personnel

access

screening,

personnel

badging, site security force manning,

compensatory

measures,

and protected

and vital area integrity.

Exterior lighting was

checked during backshift inspections.

II

No violations or deviations

were identified.

~

~

ll.

Licensee

Event

Re ort Follow-u

92700

Status of LERs

The

LERs identified below were also closed out after in-office review and

follow-up inspections

were performed

by the inspectors

to verify licensee

corrective actions:

Unit 1:

87-06 (Rev.l), 88"17, 88-21, 88-23, 88-24, 88-24

(Rev.l), 89-01, 89-04, 84-40,

87-23 (Rev. 1), 88-04,

88-26, 88-26 (Rev. 1), 88-28 (Rev. 1), 89-02, 89-03, 88-32

and Special

Report 89-01.

Unit 2:

88-06, 88-09, 88-21, 88-21 (Rev.

1) 88-22,

88-22 (Rev. 1),

89-03, 87-21, 88-10,

88-13 (Rev. 1), 88-12, 89-01, 89"Ol

(Rev.

1) and 88-25.

No violations or deviations

were identified.

12.

0 en Item Follow-u

92703

92702

a.

Ade uac

of Root Cause

Evaluation for Ino erable

Over ower

Differential

Tem erature

OPDT

Channel

Unresolved

Item

50-275/88-21-01

Closed

As noted in the cover letter of Inspection

Report 50-275/88-21,

the

statement that "no corrective actions to procedures

or training were

17

recommended"

in

LER 1-88-21 was not acceptable.

The inspection

report documented

the licensee's

commitment to submit

a revision to

the

LER to provide clarification of root cause

and corrective

actions.

On November 14,

1988, the licensee

submitted

a revision to

LER 1-88"24.

The revised

LER provided acceptable clarifications to the root cause

evaluation

and the analysis of the event.

Corrective actions

described

were more detailed than Revision

0 of the

LER, specifying

functional testing

and training requirements

ss well as procedure

changes.

These

wer e found to be acceptable.

The item was determined to be unresolved

in Inspection

Report

50-275/88-21

based

on the lack of corrective actions

taken in

response

to a Technical Specification violation. It was

subsequently

determined that the licensee's

nonconformance

process

had not been completed

and the

NCR review chairman stated that

appropriate corrective actions

were being actively considered

at the

time of issuance

of the

LER.

The inspector discussed

with plant

management

that, in situations

such at this one,

a note is needed

in

the

LER that the review of an event

has not been

completed

and

a

revision is forthcoming.

Based

on the corrective actions described

in the

LER this item is closed.

This also completes

the review of

revisions

0 and

1 of LER 50-275/88-24.

b.

Main Steam

Line Seismic Restraint'no

erable

Due to Inade uate

Confi uration

Mana ement

Follow-u

Item 50-323/ 87-43"Ol

Closed

This follow-up item incident concerned

a main steam line seismic

restraint that was modified and left inoperable in an operational

mode in which the line was required to be operable.

The primary

issue of the event was that work had

been

approved which affected

the op'erabi lity of equipment

by affecting its seismic qualification.

The inspector

reviewed the licensee's

corrective actions

and found

that they acceptably

addressed

the issues

of the incident.

However,

continued

instances

where work affects

equipment seismic

qualification in modes

where the equipment is required to be

operable

continued to be an issue.

An example of this was the work

performed

on plant vent ducting as described

in the January

1989

team inspection report 50-275/89-01.

In addition, the configuration

management

program,

which the licensee

maintained will address

the

issues of maintaining the design basis in its initial stages.

Therefore, while Follow-up Item 50-323/87-43-01 is closed,

the

inspector will review these

issues

in future inspections

as

follow-up to the open items contained in Inspection

Report

50-275/89"01.

30703

On May 5, 1989,

an exit meeting

was conducted with the licensee's

representatives

identified in paragraph

1.

The inspectors

summarized

the

scope

and findings of the inspection

as described

in this report.

Licensee

acknowledged

the concerns

and findings in the inspection report.