ML15239A069
| ML15239A069 | |
| Person / Time | |
|---|---|
| Site: | Oconee |
| Issue date: | 07/13/1993 |
| From: | NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II) |
| To: | |
| Shared Package | |
| ML15239A068 | List: |
| References | |
| 50-269-93-11, 50-270-93-11, 50-287-93-11, NUDOCS 9308050088 | |
| Download: ML15239A069 (46) | |
See also: IR 05000269/1993011
Text
ENCLOSURE
INITIAL SALP REPORT
U. S. NUCLEAR REGULATORY COMMISSION
REGION II
SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE
INSPECTION REPORT NUMBERS
50-269/93-11, 50-270/93-11 AND 50-287/93-11
DUKE POWER COMPANY
OCONEE UNITS 1, 2 AND 3
FEBRUARY 2, 1992 THROUGH MAY 1, 1993
9308050088 930713
ADOCK 05000269
G
PDR_
TABLE OF CONTENTS
Page
I.
INTRODUCTION.
..................................... 2
II. SUMMARY OF RESULTS................................. 2
III.
CRITERIA.
......................................... 4
IV. PERFORMANCE ANALYSIS................................. 4
A.
Plant Operations
............................. 4
B.
Radiological Controls ......................... 6
C.
Maintenance/Surveillance ....................... 9
D.
Emergency Preparedness........................11
E.
Security ....
............................12
F.
Engineering/Technical Support .................. 14
G.
Safety Assessment/Quality Verification..........16
V.
SUPPORTING DATA AND SUMMARIES ....................... 17
A.
Licensee Activities..........................17
B.
Direct Inspection and Review Activities............18
C.
Escalated Enforcement Activities ...............18
D.
Management Conferences........................19
E.
Confirmation of Action Letters.................19
F.
Reactor Trips/Unplanned Shutdowns..............20
G.
Review of Licensee Event Reports...............21
H.
Licensing Activities....
.....................21
I.
Enforcement Activity.........................22
2
I.
INTRODUCTION
The Systematic Assessment of Licensee Performance (SALP) program is an
integrated NRC staff effort to collect available observations and data on a
periodic basis and =to evaluate licensee performance on the basis of this
-information. The program is-supplemental to normal regulatory processes used
- to ensure compliance with NRC rules and regulations. It is intended to be
sufficiently diagnostic to provide a rational basis for allocation of NRC
resources and to provide meaningful feedback to the licensee's performance in
each functional area.
An NRC SALP Board, composed of the staff members listed below, met on June 8,
1993, to review the observations and data on performance, and to assess
licensee performance in accordance with the guidance in NRC Manual Chapter
NRC-0516, "Systematic Assessment of Licensee Performance". The Board's
findings and recommendations were forwarded to the NRC Regional Administrator
for approval and issuance.
This report is the NRC's assessment of the licensee's safety performance at
the Oconee Units 1, 2 and 3 for the period February 2, 1992, through May 1,
1993.
The SALP Board for Oconee was composed of:
J. R. Johnson, Deputy Director, Division of Reactor Projects (DRP),
Region II (RH), (Chairman)
J. P. Jaudon, Deputy Director, Division of Reactor Safety (DRS), RH
J. P. Stohr, Director, Division of Radiation Safety and Safeguards
(DRSS), RII
A. R. Herdt, Chief, Reactor Projects Branch 3, DRP, RH
D. B. Matthews, Director, Project Directorate 11-3,
Office of Nuclear Reactor Regulation (NRR)
L. A. Wiens, Project Manager, Project Directorate 11-3, NRR
P. E. Harmon, Senior Resident Inspector, Oconee, DRP, RH
Attendees at SALP Board Meeting:
M. S. Lesser, Chief, Reactor Projects Section 3A, DRP, RH
W. H. Miller, Jr., Project Engineer, Reactor Projects Section 3A, DRP, RII
W. K. Poertner, Resident Inspector, Oconee, DRP, RH
R. L. Watkins, Project Engineer, Reactor Projects Section 3A, DRP, RH
II. SUMMARY OF RESULTS
Oconee was operated safely during the assessment period. This included
improvement in shutdown operations. Effective command and control over plant
evolutions was exercised. Weaknesses remained in configuration control and
procedural usage. The previously established organizational structure
impaired effective oversight of Keowee by nuclear operations. Following the
loss of offsite power event of October 1992, Keowee was reorganized, and
programs for operator standards and training were developed.
3
Performance in the radiological protection area was superior. The ALARA
program remained strong. The water chemistry and the environmental and
effluent monitoring programs were effectively implemented. The organization
was stable, and the radiological training program was good. Deficiencies were
identified with radioactive material labeling, area posting and adherence to.
radiological control area access procedures.
Preventive and predictive maintenance programs were effectively developed and
implemented. These, along with management efforts to reduce existing backlogs
of work requests and temporary modifications, improved plant equipment
performance. Inadequate controls over maintenance and surveillance activities
contributed to several operational events which included reactor trips and the
October 1992 Loss of Offsite Power event.
Management commitment to the emergency response organization was evident as
the program remained strong. The response team was aggressively exercised
with numerous drills and challenging scenarios. Emergency facility equipment
was well maintained, and a siren system upgrade was fully implemented.
The security program was well managed and supported. Personnel were
effectively trained and knowledgeable of duties and responsibilities.
Initiatives were taken to review fully all operability aspects of a support
facility in order to provide appropriate security measures. Discrepancies
were conservatively documented and addressed. Improvement was noted late in
the assessment period with closed circuit television reliability.
Engineering provided good support for plant modifications, outages and
maintenance. Engineering personnel were knowledgeable and demonstrated a high
degree of ownership over their respective systems. Weaknesses existed in
resolving emergent issues and with system flow model calculations.
Performance in the operator requalification program declined from the previous
assessment period due to weaknesses in examination content and evaluator
techniques.
In the area of Safety Assessment/Quality Verification, performance was
inconsistent. Management was thorough and conservative when addressing
issues recognized as clearly safety significant and licensing submittals.
Corrective actions to improve shutdown risk and command and control of
operating evolutions were effective. A questioning attitude towards suspect
test results was not always evident, and management was slow to recognize the
need for increased oversight of Keowee operations.
4
Overview
Performance ratings assigned-for the last rating period and the current period
are shown below.
Rating Last Period
Rating This Period
Functional Area
8/01/90- 2/01/92
2/02/92 - 5/01/93
Plant Operations
2
2
Radiological Controls
1
1
Maintenance/Surveillance
2
2
1
1
Security
1
1
Engineering/Technical
Support
2
2
Safety Assessment/
Quality Verification
2
2
III.
CRITERIA
The evaluation criteria which were used to assess each functional area are
described in detail in NRC Manual Chapter MC-0516, which can be found in the
Public Document Room files. Therefore, these criteria are not repeated here,
but will be presented in detail at the public meeting to be held with licensee
management on July 28, 1993.
IV. PERFORMANCE ANALYSIS
A.
Plant Operations
1.
Analysis
This functional area addresses the control and performance of activities
directly related to operation of the facility.
During the previous SALP assessment, weak or deficient operator
attention and control of evolutions during outage conditions was
identified. During this assessment period, command and control of
operations activities improved particularly during shutdown conditions.
Configuration control errors and mispositioned equipment events
continued to occur. Procedural inadequacies, usage weakness and
inattention to detail contributed to several operational events.
Although improvement was achieved in the area of command and control
over licensed activities, there were occasions which demonstrated that
continued efforts are needed. In one case a procedure review was
inadequate when the task was inappropriately delegated. On another
occasion, operators permitted maintenance activities during low power
physics testing, which resulted in an inadvertent cooldown.
5
Operator response to transients and upset conditions was good. Prompt
action by operators prevented over-pressurization of the quench tank
during a system misalignment. Several transients requiring operator
action were handled effectively. Operators generally demonstrated
excellent knowledge of plant systems and processes. Fundamental
watchstanding practices improved from last assessment period. Shift
turnovers were thorough. Preshift meetings and mid-shift Operations
Department update meetings provided effective communications to both
operations personnel and other plant support groups. Log keeping was
adequate, but amplifying details regarding evolutions were inconsistent.
Shift staffing exceeded Technical Specification requirements without the
need of excessive overtime. Operators properly used Abnormal Procedures
and Emergency Operating Procedures when required.
Operators were not required to have extensive knowledge of Keowee
operations. This became evident during the loss of offsite power event
in October 1992. The operators' response to and recovery from this
event was complicated by the lack of appropriate procedural guidance and
overall complexity of the various electrical power system interactions.
Adequate standards had not been established for Keowee operator
performance, duties, responsibilities and knowledge levels. Keowee
operations and management structure was subsequently reorganized to
report to Oconee Nuclear Operations Department.
Performance standards
for Keowee operations were established and implemented towards the end
of this assessment period. Also, some limited training of Oconee
operators on Keowee systems was initiated late in this assessment
period.
Configuration control and procedural adherence exhibited weaknesses that
represented a continuation of problems identified during the last SALP
period. Mispositioned equipment incidents continued to occur during
this evaluation period. Failure to follow approved procedures occurred
in several instances. In some cases procedural requirements and
policies were not clearly understood by personnel.
Procedural steps
were inappropriately marked "Not Applicable" (NA) without a thorough
review and resulted in a violation of Low Temperature Over-pressure
Protection requirements and an inadvertent draining of a portion of the
main feedwater system. Guidance on marking steps NA was implemented
midway in the period and some improvements were noted.
Other examples
included the use of the wrong unit's procedure to calculate an estimated
critical position and a failure to follow a procedure that resulted in
misplaced fuel assemblies during refueling. In one instance, an
Abnormal Procedure for restoring offsite power was considered
inadequate.
Both operators and supervisory personnel exhibited a conservative
approach to technical issues. The Operations Support Group was
instrumental throughout the period in providing both technical and
administrative support to the control room. Work control screening,
outage scheduling and review, and procedure review and revision were
also effectively performed by this group. The Operations Support Group
was staffed primarily with licensed senior reactor operators (SROs) and
reactor operators (ROs). The experience level of both control room
personnel and the Operations Support Group were considered very high.
6
Management continued to work toward the "black board" concept and
improvement was noted by a reduction in the number of lit annunciators
and nuisance alarms. Plant equipment labeling efforts have reduced the
instances of wrong unit or wrong equipment events. Control room
drawings were maintained legible, however, changes resulting from minor
modifications were not always promptly reflected.
Operator attention and control of evolutions during shutdown conditions
improved from the previous assessment period. Management implemented
changes to control room supervisory functions, and defined operator
duties during shutdown conditions. These changes were in response to
several significant events in the previous evaluation period. Control
room decorum and professionalism improved. More formal communications
resulted in a decrease in the number of events. The duties and
responsibilities of the Operator at the Controls were revised to allow
concentration on plant status and evolutions in progress.
Administrative duties and support activities were assigned to other
personnel.
These changes were effective and contributed to improved
performance during shutdown activities.
One Severity Level 3 Violation and nine Severity Level 4 Violations were
identified.
2.
Performance Rating
Category: 2
3.
Recommendations
The Board noted that problems associated with inadequate procedures and
failure to follow procedures continued from the previous SALP period.
Management corrective actions to address this weakness have not been
fully effective. A broad review of procedural usage should be
undertaken to identify the underlying causes.
B.
Radiological Controls
1.
Analysis
This functional area addresses those activities related to radiation
safety, radiological effluent control and monitoring and
primary/secondary chemistry control.
The licensee continued to maintain a stable and well-qualified radiation
protection staff with no significant changes made to the licensee's
radiological controls organization. The licensee's training program
remained sufficient during the period with program enhancements that
included instructions to plant workers and the revisions to 10 CFR Part
20, as well as the implementation of an Electronic Dose Capture System
and its interface with digital alarming dosimeters (DADs). Early in the
assessment period, continuing training was not being provided for
contract health physics (HP) technicians. The licensee corrected this
by adding training modules focusing on refresher HP theory and practices
and providing additional training to the contract HP technicians.
7
The licensee's program to maintain overall occupational external
exposure as low as reasonably achievable (ALARA) remained very good.
The collective dose for 1992 was 217 person-rem per unit. The
collective dose in 1993 to the end of the SALP period was 24 person-rem
per unit. During the assessment period,-the licensee initiated and
completed replacement of the letdown piping and "J" leg drains from the
steam generators in Units 1 and 3. Replacing this highly radioactive
piping with new piping, thereby reducing high-dose rates in the
containment basement areas, was a significant ALARA initiative.
The internal exposure controls, i.e., contamination control, the
respiratory protection, and the bioassay program, were effectively
implemented to control exposure. No exposures exceeded regulatory
limits.
Licensee performance in the contamination control area continued to be
effective in ensuring that contaminated floor space and personnel
contamination events were maintained below established goals and were
trending down. Contaminated space was typically controlled to less than
seven percent of the radiologically controlled area (RCA).
Personnel
contamination events did not result in any skin doses or intakes greater
than regulatory limits.
During the assessment period, repetitive problems were identified with
radioactive material control practices. Specifically, the NRC
identified:
(1)
recurring instances of radioactive material in the RCA
not being properly labeled as such, and (2) recurring instances of areas
in the RCA containing radioactive material not being properly posted.
As a result of the licensee's investigation of a possible skin dose
overexposure to a radwaste operator, the licensee found that the worker
rarely used the Electronic Dose Capture System to log into the RCA of
the plant. Further investigation revealed that approximately 20 percent
of. personnel working in the RCA were not logged in any radiation work
permit (RWP). This indicated less than fully effective adherence to
procedures and control of work being conducted in the RCA.
During the assessment period, the licensee's audit program was effective
in identifying radiological control program deficiencies. However, the
effectiveness of the audit program was reduced because corrective
actions to findings were not properly implemented. Specifically, of 23
problem identification reports reviewed, 17 had no corrective actions
assigned for deficiencies identified, including several which were
nearly a year old. Furthermore, out of 47 radiological deficiencies
reviewed, all but one were assigned the lowest priority for correction.
Typical issues not resolved included procedural inadequacies, non-ALARA
work practices, and miscellaneous dosimetry problems.
The licensee's performance with regard to maintaining low levels of
radiation doses from effluents was good. The whole body doses were less
than one millirem/year each from the liquid effluents and from the
gaseous effluents released during 1992. Those doses were a small
percentage of their respective limits. Compared to 1991, larger volumes
of liquid radwaste, with higher radionuclide concentrations, were
processed through the liquid radwaste treatment systems during 1992.
8
Although the amount of activity released increased slightly, a small
decrease in the total body dose from liquid effluents for 1992 was
achieved by a reduction of the Cs-137 concentration in the effluent. By
processing laundry waste water through powdered resin before release,.
the Cs-137 concentration in the effluent was significantly reduced.
There was one unplanned release during 1992 which occurred when
approximately 2000 gallons of slightly contaminated water from the Low
Pressure-Service Water System were inadvertently discharged from the
Unit 2 Low Pressure Injection Cooler to Lake Keowee. No release limits
were exceeded during that event.
Effluent radiation monitor performance was mixed. A longstanding
problem with the Low Pressure Service Water (LPSW) monitors was
corrected and the monitors for Units 1 and 2 were returned to service
during the assessment period. System modifications were required to
correct insufficient sample flow from all portions of the LPSW system.
The modification for the Unit 3 system was completed during the previous
assessment period. Late in the assessment period there were two monitors
that were inoperable for several days before the licensee detected that
they were not functioning properly. Weaknesses were identified with the
licensee's corrective actions for restoring the monitors to an operable
status.
The licensee's environmental monitoring program was effectively
implemented. The program results for 1992 indicated that there was no
significant radiological impact on the health and safety of the general
public resulting from plant operations. Dose estimates calculated from
environmental monitoring program data were in reasonable agreement with
dose estimates calculated from effluent release data and were well
within 40 CFR 190 dose limits. The licensee's performance in the
Environmental Protection Agency's interlaboratory crosscheck program
indicated that an effective quality assurance program had been
maintained for analysis of environmental samples.
The parameters required to be monitored as part of the water chemistry
control program were maintained well below their technical specification
(TS) limits. The program also included provisions for implementing,
with few exceptions, industry guidelines for PWR primary and secondary
water chemistry. The activity of reactor coolant was also maintained
well within the TS limits. The activity was slightly higher in the Unit
3 coolant than in Units 1 and 2 coolant due to residual contamination
from leaking fuel in previous fuel cycles. The licensee has since
implemented a policy of reloading fuel with zero defects with regard to
leaking fuel.
There were no transportation incidents involving the licensee's
shipments of radioactive material during the assessment period. The
program was effectively implemented and provided for preparation and
shipment of radioactive material pursuant to the Department of
Transportation's regulations.
9
Five Severity Level 4 Violations were identified.
2.
Performance Rating
Category: 1
3.
Recommendations
None
C.
Maintenance/Surveillance
1.
Analysis
This functional area addresses those activities related to equipment
condition, maintenance, and surveillance testing. In addition to the
routine inspections in this area, an Electrical Distribution System
Functional Inspection (EDSFI) was conducted during this assessment
period.
The licensee's performance in the maintenance/surveillance functional
area was inconsistent throughout the assessment period. Predictive
maintenance and equipment monitoring was aggressively pursued and was
effective whereas weaknesses were noted in areas such as procedural
adherence, documentation of problems during troubleshooting and repairs,
and maintenance/surveillance induced reactor trips and transients.
The licensee continued to focus efforts on preventative maintenance.
The thermography program introduced during the previous SALP period was
effective in identifying potentially significant maintenance problems
prior to failure and was effective in identifying leaking valves.
Management efforts were effective in significantly reducing the
maintenance work request backlog. The backlog was maintained at levels
which'were better than management expectations. This contributed to
improved equipment reliability as only one reactor trip from power was
caused directly by equipment failure. Improved controls and efforts to
reduce temporary modifications have also been successful.
The maintenance department was well staffed with experienced and
knowledgeable personnel.
The use of vendors and contractors was
controlled with most maintenance support performed by Duke Power
individuals. Plant material condition and routine housekeeping was
adequate.
During this period, significant operational problems were attributable
to poor maintenance controls. A loss of offsite power event and reactor
trip occurred in October 1992 due to maintenance activities conducted in
the 230 kilovolt switching station control power system. Three other
reactor trips from power occurred during maintenance activities. These
were due to problems during troubleshooting or repair activities and use
of a wrong wiring diagram. Although three refueling outages were
conducted and adequately managed, three unit shutdowns were required
during the period due to inadequately performed maintenance.
10
Problems with independent verification, undocumented work activities and
other poor maintenance practices continued to occur during the period.
Examples include an inadvertent reactor protection system channel
actuation due to performing a surveillance on the wrong unit, improper
wire terminations that were "verified" by two technicians and a Quality
Control inspector, an undocumented activity involving lifting leads and
an Emergency Feedwater Actuation due to poor scaffolding controls.
Surveillance activities caused a unit runback and testing on the wrong
unit caused a plant trip.
The test program for the Keowee Hydrostation did not adequately
demonstrate the ability of the system to perform its design function. A
periodic test had not been performed on the Keowee units to supply power
through the overhead path. Additionally relays required to isolate
portions of the switchyard and to transfer Keowee auxiliary power to an
alternate source were not fully tested. Also, as discussed Section
IV.F. (Engineering/Technical Support), LPSW testing had not been
adequately performed to validate flow model calculations until the NRC
.pointed-out errors in the model.
In other areas, several inadequate
surveillance procedures were identified during the period including one
The licensee's inservice inspection (ISI) program was effectively
implemented during this inspection period.
ISI non-destructive
examinations were conservatively performed. The procedures, examination
techniques, and documentation of results were good. Personnel were
knowledgeable in their areas of responsibility. Some problems were
identified involving the failure to document and resolve welding
discrepancies identified by the vendor on ASME Code relief valves and an
untimely and inadequate relief request from postmodification hydrostatic
testing.
Seven Severity Level 4 Violations were identified.
2.
Performance Rating
Category: 2
3.
Recommendations
A significant number of plant transients were attributed to inadequate
maintenance or surveillance activities. Some of these were related to
procedural problems and work controls. A broad review of procedures,
similar to that mentioned in the Operations functional area is
recommended.
11
D.
1.
Analysis
This functional area addresses activities related to the execution of
the Emergency Plan and its implementing procedures, including licensee
performance during emergency exercises and actual events, interactions
between onsite and offsite emergency response organizations during
emergency exercises and actual events, and support and training of
onsite and offsite emergency response personnel.
Management support and involvement in the emergency preparedness (EP)
program was evidenced by the numerous drills conducted and the emergency
facility and equipment improvements made during the assessment period.
The licensee continued to administer an aggressive schedule of EP
training drills, creating challenges for the emergency response
organization (ERO) that exceeded the training requirements of the
Emergency Plan. These drills (two of which were conducted during off
hours) included annual participation by each of the five Operations
shifts in simulator-driven exercises involving the full ERO. This
approach, combined with formal classroom training, appeared to be an
effective way of maintaining organizational readiness for responding to
an emergency.
The onsite emergency preparedness staff was qualified and continued to
provide comprehensive emergency preparedness training. Offsite support
agency training for fire, ambulance, rescue, hospital, and local law
enforcement agencies was conducted in accordance with commitments in the
Emergency Plan and agreement letters with assisting agencies.
During the annual exercise in August 1992, the licensee demonstrated its
capability to provide for the health and safety of the public by
effectively implementing the Emergency Plan in response to the simulated
accident scenario. The scenario appropriately challenged the licensee's
ERO, and included full participation by the NRC. The licensee
demonstrated the ability to identify emergency conditions, to make
correct classifications in accordance with Emergency Plan implementing
procedures, to take appropriate measures to mitigate the adverse
consequences of degrading plant conditions, and to recommended
appropriate protective actions for the public. The emergency response
facilities were activated fully within the required time periods. The
timely activation and capable functioning of the Emergency Operations.
Facility constituted an exercise strength. An exercise weakness was
identified for failure of the Joint Information Center to quantify or
put into perspective, for the general public, a radiological release
which occurred as a component of the scenario.
The licensee maintained emergency facilities, equipment, instrumentation
and supplies in a state of readiness with thorough equipment
inventories, surveillances, and functional tests. Just prior to the
beginning of the assessment period, the licensee fully implemented an
upgrade of the offsite siren system through the addition of a
computerized feedback capability for monitoring each siren's operation
during any mode of testing or actual activation. This resulted in very
12
high siren availability (approximately 99 percent) during 1992, with the
feedback system successfully identifying siren operability problems for
prompt corrective action.
The 1991 corporate reorganization necessitated major EP program changes
which were implemented during the assessment period. Most of the EP
program responsibilities-previously held by the corporate staff were
transferred to the site. Concurrent with this transfer of
responsibility was the relocation of many emergency response personnel
to the site. Some organizational functions were also shifted from the
Emergency Operations Facility to the Technical Support Center. However,
the totality of the functions performed did not change with the
reorganization, and adequate emergency response capabilities were
maintained.
During this assessment period, the licensee's Emergency Plan was
activated twice at the Notification of Unusual Event level.
Each of the
events was properly classified, and notifications to State and local
governments and the NRC were made in accordance with applicable
requirements.
One Severity Level 5 Violation was identified.
2.
Performance Rating
Category:
1
3.
Recommendations
None
E.
Security
1.
Analysis
This functional area addresses those safeguards activities related to
the protection provided to the station's safety related vital equipment,
and the assurance that individuals authorized station access are fit for
duty.
The licensee's safeguards program was well managed at the site level as
evidenced by the professionalism and effectiveness of its proprietary
security force. Officers were well trained, knowledgeable of their
duties and responsibilities, well versed in their procedures, and
adequately equipped. Shifts were appropriately staffed.
The licensee conducted effective quality assurance audits which were
thorough and complete. Corrective actions for the audit findings were
timely and appropriate.
As noted in previous SALP assessments, the licensee's closed circuit
television system, used to assess protected area barrier alarms,
continued to be non-operational in several zones. Several television
13
monitors located inside the alarm stations were frequently out of
service. Thus, the licensee continued to use compensatory measures to
meet its Plan commitments during the period. Toward the end of the SALP
period, camera assessment system reliability had greatly improved.
The licensee completed an engineering evaluation of certain non-vital
piping which, given various operational modes and valve lineups, could
be important to safety and therefore should be protected. This
licensee's initiative in conducting this review was well coordinated
with the NRC and adequate compensatory measures have been implemented
where necessary.
With respect to other elements of the safeguards program, access
controls and alarm station operations were appropriate, barriers and
alarms were maintained as required, lighting was sufficient, and (except
as noted earlier regarding cameras) maintenance and compensatory
measures were adequate.
During this SALP period, the licensee identified several security events
involving inadequate communications. A failure by the Control Room
operators to notify the security shift that a facility important to
safety was not operable resulted in the failure to institute timely
compensatory actions. A failure by Human Resources personnel to notify
the security shift of a positive drug test resulted in an unauthorized
access to the Station. Also identified by the licensee was its failure
to conduct daily communications tests as committed to in its Security
Plan. These were appropriately documented in the Safeguards Event Log.
In addition, the NRC identified several Plan inaccuracies relative to
the Turbine Building security barrier. The licensee took appropriate
corrective actions for the aforementioned events.
The licensee has clarified its generic Corporate Procedure for Reporting
Safeguards Events to ensure that NRC reporting criteria is met. This
has resulted in an overall increase in reporting events in the
Safeguards Logs.
No violations were identified.
2.
Performance Rating
Category: 1
3.
Recommendations
None
14
F.
Engineering/Technical Support
1.
Analysis
This functional area addresses activities associated with the design of
plant modifications and of technical support for operations, outages,
maintenance, licensed operator training and requalification.
Engineering support was strongest in support of plant operations and
planned outages. Weaknesses were evident in the response to emergent
issues not directly related to operability and in corrective actions.
Licensed operator training improved, but some weakening of the
requalification program was evident. The staffing of the engineering
organizations was satisfactory.
Engineering support for plant modifications was adequate. The quality
-and .technical content of temporary and minor modifications was generally
good. Examples included the addition of Vent Valve ICCW-422, relocation
of IC-850 and IC-852, and snubber additions on main feedwater and
emergency feedwater piping. There were also instances found of
inadequate design calculations and reviews, although some of the
inadequacies occurred before this assessment period. Examples included
previous and current Low Pressure Service Water (LPSW) flow model
calculations used to justify operability of the system. After the NRC
identified the errors, the licensee corrected them and then tested the
LPSW to verify operability. The tests demonstrated that the LPSW
systems were degraded in that excessive flow through the low pressure
injection coolers could be achieved under certain design basis
conditions and that LPSW flow through the reactor building cooling units
could be significantly below the assumed accident condition -flow rate.
The flow testing conducted on Unit 3 also identified that the system was
degraded due to a mispositioned valve. Single failure vulnerabilities
were also identified in the design basis documentation previously
conducted.
The licensee's engineering and technical support have been responsive to
station needs. Examples include identification and prompt communication
to the NRC of the need to change a prior commitment relating to post
accident boron dilution flow monitoring, modifications to correct
degraded control voltage to the "S" and "E" breakers, corrective action
for inadequate Keowee auxiliary breaker closing power, and modifications
to the Standby Shutdown Facility makeup pump accumulators. Engineering
has generally provided prompt and well-founded solutions to short-term,
operational problems. The response to other issues in which immediate
operability was not an issue has not been quick or as thorough.
Examples include problems with Keowee X-relays, numerous LPSW issues
(raised by the NRC), and a revised response to NRC Bulletin 88-04
concerning the deadheading of LPSW pumps. Also, the planning for the
replacement of switchboard batteries did not identify potential problems
with operating a battery charger without a connected battery. This
resulted in a loss of offsite power and a reactor trip to Unit 2.
System engineers assumed "ownership" of their assigned systems and
15
actively participated in the resolution of problems. Component
engineering provided good support to maintenance.
Engineering support for the resolution of other emerging issues, not
identified as requiring immediate corrective action, was sometimes
deficient. Examples of problems noted included: (1) the failure to
perform a safety-evaluation for a temporary modification (installation
of an electrical jumper on radiation monitor interlock to Valve 2LWD-2);
(2) the use of incorrect design drawings in the completion of a plant
modification (resulting in a reactor trip); (3) an inadequate
engineering evaluation of the operability of a letdown storage tank
check valve; (4) failure to take prompt and adequate corrective actions
for low indicated service water flow through the 3B Low Pressure
Injection (LPI) Coolers; and (5) failure to correct the MG-6 testing
deficiency after identification during Keowee Unit 2 testing.
An Electrical Distribution System Functional Inspection revealed
problems in testing, design analyses, and design basis documentation.
Similar problems were also found in the Oconee emergency AC power
source. These problems resulted in part from the lack of a thorough
understanding of the design basis of the site's electrical distribution
system.
Operator training was effective.
Improvements were noted in the initial
training of licensed operators. This good performance was indicated by
the successful completion of all seven candidates nominated for licenses
in January 1993. The candidates exhibited good communications and
interactions during their simulator examinations, but had a generic
weakness in radiation protection. The previously noted problems with
simulator fidelity to the plant have been rectified. The performance of
requalification was satisfactory. During the June 1992 requalification
examination, five of six crews and 22 of 24 operators passed.
Weaknesses noted included the content and construction of the written
test and poor or improper cuing during the job performance measures.
This was in contrast to the strong performance of facility evaluators
during the previous assessment period.
Two Severity Level 4 Violations were identified.
2.
Performance Rating
Category: 2
3.
Board Recommendations
None
16
G.
Safety Assessment/Quality Verification
1.
Analysis
This functional area addresses those activities related to the
licensee's implementation of safety policies related to license
amendments, exemptions and relief requests; responses to Generic
Letters, Bulletins and Information Notices; resolution of safety issues;
reviews of plant modifications performed under 10 CFR 50.59; safety
review committee activities; and the use of feedback from self
assessment programs and activities.
Management performance in the area of safety assessment and quality
assurance was inconsistent. Efforts to correct weaknesses in command
and control were effective, however many repetitive problems continued
in the area of procedural compliance by personnel.
Prompt followup to
deficiencies was not always evident. Licensing documentation and
submittals were generally very good.
Management implemented several corrective actions to improve the
operation of the station in areas previously identified by the NRC as
weak or deficient. Improved performance was noted in shutdown risk and
control room command and control. Initiatives to improve the conduct of
outage activities and the reduction in shutdown risk vulnerability were
noteworthy. Of particular note was the reduction in control room
distractions, efforts to more fully inform employees of outage
activities, and an independent safety assessment of the outage schedule.
The Nuclear Safety Review Board was objective and thorough in its review
of operations and problems at Oconee. Management was responsive.to the
comments and recommendations from the Board.
In the area of Keowee operations and design, management was slow to
recognize the need for corrective action to address previously
identified NRC concerns and weak areas. In September 1992 a management
meeting was held at NRC request to discuss these issues. The licensee
indicated that while some changes to procedures were appropriate, major
operational, organizational and procedural changes were not necessary.
However, in October 1992, a loss of off site power event occurred and
followup inspections identified significant weaknesses in these areas.
It should be noted that the licensee's Significant Event Investigation
Team, dispatched to site to review the event, was effective in
determining root causes, safety implications and provided
recommendations for corrective action.
Following these inspections, a
comprehensive Emergency Power Management Plan was developed. This plan
was intended to substantially improve the overall operation and
maintenance of the Keowee facility. An organizational change was also
made to incorporate the Keowee station under Oconee station line
management.
At the conclusion of this assessment period the
effectiveness of these changes remained under evaluation.
Issues which the licensee recognized as clearly safety significant were
normally resolved aggressively. Actions were conservative and thorough,
and involved early interaction with the staff. Examples included 100
per cent steam generator tube inspection, corrective action for degraded
17
control voltage for "E" and "S" breakers and corrective actions related
to the emergency electrical system after the Unit 2 Loss of Power event.
At times, the failure to further probe into questionable indications led
to untimely identification of adverse conditions. Examples included the
failure to investigate abnormal LPSW flow during valve testing and
failure to promptly investigate abnormal position indication on a Keowee
breaker. Management efforts to address the large number of operator
errors and procedure violations have not been fully effective as they
continued to occur in a number of areas in the plant.
A significant improvement was noted in the quality and timeliness of
Inservice Inspection and Testing relief requests since the last
evaluation period. Most amendments and relief requests were processed
without the need for additional clarifying information or supplements to
the original submittal.
When additional information was required, the
licensee was very responsive in providing the requested information
promptly.
The licensee provided responses to NRC requests within the time frame
requested or provided written notification if circumstances prevented
meeting the requested schedule. These responses were generally clear,
precise, and sufficient. Examples include responses to Generic Letter 91-11, Vital Instrument Busses and Tie Breakers, Generic Letter 88-20,
Independent Plant Examinations, and Generic Letter 87-02, Seismic
Qualification of Mechanical and Electrical Equipment in Operating
Plants. However, in one instance, an inadequate response to Bulletin
88-04, Safety Related Pump Loss, was not corrected until NRC requested a
revised response.
Licensee Event Reports (LERs) in most cases were timely and well
written. One report, LER 269/92-12, concerning various problems with
the Unit 1/2 LPSW system, was submitted late.
Two Severity Level 3 Violations and two Severity Level 4 Violations were
identified.
2.
Performance Rating
Category:
2
3.
Recommendations
None
V.
SUPPORTING DATA AND SUMMARIES
A.
Licensee Activities
A major reorganization was announced in November 1991, including relocating
Design Engineering to the site. Implementation of the reorganization was
completed in July 1992. Additional management changes during this assessment
period included the April 1, 1993, reassignment of Mr. R. L. Sweigart, former
18
Superintendent Operations, to Superintendent Work Control and Mr. G. E.
Rothenberger, former Superintendent Work Control, to Superintendent Operation.
There were three refueling outages during this assessment period. Refueling
outages were completed in March 1992 for Unit 2, September 1992 for Unit 3,
and January 1993 for Unit 1. These outages were satisfactorily completed with
no major problems.* However, the Unit 3 refueling outage required extensive.
decontamination activities due to the contamination which occurred inside
Unit 3 Containment following the November 23, 1991, break of a 3/4-inch tubing
connector on the Reactor Coolant System. During the Unit 1 refueling outage,
a larger than normal number of degraded steam generator tubes were identified
which were required to be plugged. This was attributed primarily to revised
tube plugging criteria.
In September 1992, the licensee determined that both trains of the Units' 1
and 2 LPI system were inoperable. The cooling water flow of the LPSW system
through the LPI heat exchangers were found to exceed the manufacturer's
specifications. The power level for both units was reduced to approximately
10 percent and modifications were made to reduce the flow through the heat
exchangers to meet the manufacturer's specifications.
On October 19, 1992, during maintenance activities, a loss of off site power
occurred for Unit 2 which was followed by a subsequent loss of the Keowee
Hydro Station.
Since this event, the licensee has placed the Keowee Hydro
Station under the Oconee management and has implemented a number of procedure
changes to improve the reliability of the emergency power supply for the
Oconee Station.
B.
Direct Inspection and Review Activities
In addition to the 36 routine NRC inspections and two initial and three
requalification examinations performed at the Oconee facility, the following
three special inspections were conducted:
December 9, 1991
February 21, 1992
Shutdown Risk Inspection
October 20 - 28, 1992
Augmented Inspection Team (AIT) Loss of
Off-site AC Power Supply
January 25 - March 5, 1993
Electrical Distribution System Functional
Inspection (EDSFI)
C.
Escalated Enforcement Activities
1.
Orders
None
2.
Civil Penalties (CP)
Two Severity Level III problem violations (IR 91-32/EA 91-167) were
issued on February 3, 1992, involving ten specific violations related to
the degradation of the decay heat removal event of September 7, 1991 and
19
the over-pressurization of the LPI system piping on September 19-20,
1991. ($125,000) Although both of these events occurred during the
previous assessment period, the violations were issued during this
assessment period on February 3, 1992.
A Severity Level III violation (EA 92-211) was issued on December 28,
1992, and involved the failure to take adequate corrective action to..
resolve a reduced Low Pressure Service Water System flow condition
through the Unit 3B Low Pressure Injection system cooler. ($100,000)
The licensee requested mitigation of the civil penalty. Subsequent to
this assessment period, an order to pay was issued which the licensee
complied with.
D.
Management Conferences
February 5, 1992: A meeting was held in Region II for Duke to discuss
the items identified during the Design Basis Documentation Program
evaluation of the Oconee electrical systems and the corrective actions
initiated on the identified problems.
June 24, 1992: A meeting was held in Region II for Duke to discuss the
shutdown risk procedures to be implemented for future Oconee refueling
outages. Also, discussed were Duke's Problem Investigation Program,
procedure adherence and configuration control programs at Oconee.
July 17, 1992:
An enforcement conference was held in Region II to
discuss the circumstances associated with the May 8, 1992, Unit 1
reactor trip in which one of the two required Emergency Feedwater System
flow paths was not operable and the operation of Unit 1 from May 11
through 24, 1992, with only one of the two Emergency Feedwater System
flow paths operable.
September 17, 1992: A meeting was held at the Oconee facility to
discuss the operation, management and maintenance of the Keowee Hydro
Station.
November 24, 1992: An open enforcement conference was held in Region II
to discuss the circumstances associated with the mispositioned valve in
the Unit 3 Low Pressure Service Water System.
March 29, 1993: A meeting was held at NRC Headquarters to discuss
electrical issues at Oconee.
Several additional meetings were held with Duke Power throughout the
assessment period to discuss a variety of other subjects including
licensing activities, safety initiatives, Oconee's self-assessment, the
Emergency Data System and the development status of a Babcox and Wilcox
digital module for use in the reactor protection system.
E.
Confirmation of Action Letters (CAL)
Following the October 19, 1992, Unit 2 reactor trip and loss of power
event, a CAL was issued to address the cause of the event. On October
26, 1992, a conference call was held and the licensee discussed
enhancements to be made to the Keowee Hydro Station and Keowee
20
operations. These commitments were documented in a letter to the NRC
dated October 27, 1992.
F.
Reactor Trips/Unplanned Shutdowns
Seven automatic reactor trips occurred. Five of these were attributed
to maintenance/surveillance activities, one to equipment failure and one
to operator error. These trips are as follows:
Unit 1
May 7, 1992: The unit experienced a reactor/turbine trip from 100
percent power due to a connector coming loose on the generator exciter
field. (Maintenance/Surveillance)
May 8, 1992: The unit tripped from 14 percent following a turbine trip
due to the loss of suction to the "lA" main feedwater pump which was
caused by pressure swings while lowering hotwell level.
(Operations)
Unit 2
October 19, 1992: The unit tripped from 100 percent power on the loss
of off-site power which occurred during switchyard battery modification
work when a battery charger was placed in service without a connected
battery. (Maintenance/Surveillance)
Unit 3
February 27, 1992: The unit tripped from 100 percent power following a
turbine trip due to human error. A technician was testing the loss of
generator stator cooling on Unit 2 which was shutdown in a refueling
outage but inadvertently performed the test on Unit 3.
(Maintenance/Surveillance)
June 24, 1992: A turbine/reactor trip occurred from 100 percent power
while technicians were replacing low pressure service water
instrumentation. A fuse blew in the Integrated Control System when an
incorrectly wired card was installed. This caused a momentary loss of
power to the steam generator water level instrumentation which resulted
in a turbine/reactor trip.
(Maintenance/Surveillance)
September 29, 1992: The unit tripped from 73 percent power due to low
reactor coolant system pressure from a defective Group 5 control rod
drive programmer. (Equipment Failure)
January 26, 1993: A turbine/reactor trip from 100 percent power
occurred due to low main feedwater pump discharge pressure which was
inadvertently caused by a technician during trouble shooting activities.
(Maintenance/Surveillance)
21
G.
Review of Licensee Event Reports (LERs)
During the assessment period, 30 LERs were analyzed. The distribution
of these events by cause as determined by the NRC staff was as follows:
Cause
Total Unit 1 Common Unit 2 Unit 3
Component Failure
5
2
3
Design
9
8
1
Construction/Fabrication
1
1
Installation
Other
2
1
1
Personnel
- Operating Activity
6
4
1
1
- Maintenance Activity
3
1
2
- Test/Calibration Activity
2
1
1
- Other
2
1
1
TOTALS
30
8
15
2
5
Notes:
1.
With regard to the area of personnel, the NRC
considers lack of procedures, inadequate procedures,
and erroneous procedures to be classified as personnel
error.
2.
The other category is comprised of LERs where there
was a spurious signal or a totally unknown cause.
3.
One Special Report was submitted. Also, two LERs were
submitted but were later rescinded. These reports are
not included in the above tabulation.
4.
The above information was derived from a review of
LERs performed by the NRC staff and may not completely
coincide with the licensee's cause assignments.
H.
Licensing Activities
During the rating period, approximately 175 active licensing actions
were submitted for the three Oconee units of which 97 were completed.
There were 33 licensing amendment requests of which 24 were completed.
22
I.
Enforcement Activity
No. of Deviations and Violations in Each Functional Area:
V
IV
III
II
I
Plant Operations
-
9
1
Radiological Controls
-
5
Maintenance/Surveillance
-
7
1
-
Security
Engineering/Technical
-
2
Support
Safety Assessment/Quality
-
2
2
-
Veri fi cation
TOTALS
1
25
3
-
NOTE:
Two of the Severity Level 3 violations and the Severity Level 5
violation were identified during the previous assessment period, but
reports were not issued until this assessment period.
ENCLOSURE
INITIAL SALP REPORT
U. S. NUCLEAR REGULATORY COMMISSION
REGION II
SYSTEMATIC ASSESSMENT OF LICENSEE PERFORMANCE
INSPECTION REPORT NUMBERS
50-269/93-11, 50-270/93-11 AND 50-287/93-11
DUKE POWER COMPANY
OCONEE UNITS 1, 2 AND 3
FEBRUARY 2, 1992 THROUGH MAY 1, 1993
TABLE OF CONTENTS
Page
I.
INTRODUCTION....
.........................
..... 2
II. SUMMARY OF RESULTS................................. 2
III.
CRITERIA
......................................... 4
IV.
PERFORMANCE ANALYSIS................................ 4
A.
Plant Operations
............................. 4
B.
Radiological Controls ......................... 6
C.
Maintenance/Surveillance ....................... 9
D.
..................... 11
E.
Security
................................... 12
F.
Engineering/Technical Support .................. 14
G.
Safety Assessment/Quality Verification.............16
V.
SUPPORTING DATA AND SUMMARIES ....................... 17
A.
Licensee Activities..........................17
B.
Direct Inspection and Review Activities............18
C.
Escalated Enforcement Activities...................18
D.
Management Conferences...................
..... 19
E.
Confirmation of Action Letters............
..... 19
F.
Reactor Trips/Unplanned Shutdowns...............20
G.
Review of Licensee Event Reports................21
H.
Licensing Activities.....
....................21
I.
Enforcement Activity..........................22
2
I.
INTRODUCTION
The Systematic Assessment of Licensee Performance (SALP) program is an
integrated NRC staff effort to collect available observations and data on a
periodic basis and to evaluate licensee performance on the basis of this
information.
The program is supplemental to normal regulatory processes used
to ensure compliance with NRC rules and regulations. It is intended to be
sufficiently diagnostic to provide a rational basis for allocation of NRC
resources and to provide meaningful feedback to the licensee's performance in
each functional area.
An NRC SALP Board, composed of the staff members listed below, met on June 8,
1993, to review the observations and data on performance, and to assess
licensee performance in accordance with the guidance in NRC Manual Chapter
NRC-0516, "Systematic Assessment of Licensee Performance". The Board's
findings and recommendations were forwarded to the NRC Regional Administrator
for approval and issuance.
This report is the NRC's assessment of the licensee's safety performance at
the Oconee Units 1, 2 and 3 for the period February 2, 1992, through May 1,
1993.
The SALP Board for Oconee was composed of:
J. R. Johnson, Deputy Director, Division of Reactor Projects (DRP),
Region II (RII), (Chairman)
J. P. Jaudon, Deputy Director, Division of Reactor Safety (DRS), RH
J. P. Stohr, Director, Division of Radiation Safety and Safeguards
(DRSS), RH
A. R. Herdt, Chief, Reactor Projects Branch 3, DRP, RH
D. B. Matthews, Director, Project Directorate 11-3,
Office of Nuclear Reactor Regulation (NRR)
L. A. Wiens, Project Manager, Project Directorate 11-3, NRR
P. E. Harmon, Senior Resident Inspector, Oconee, DRP, RII
Attendees at SALP Board Meeting:
M. S. Lesser, Chief, Reactor Projects Section 3A, DRP, RII
W. H. Miller, Jr., Project Engineer, Reactor Projects Section 3A, DRP, RII
W. K. Poertner, Resident Inspector, Oconee, DRP, RH
R. L. Watkins, Project Engineer, Reactor Projects Section 3A, DRP, RII
II. SUMMARY OF RESULTS
Oconee was operated safely during the assessment period. This included
improvement in shutdown operations.
Effective command and control over plant
evolutions was exercised. Weaknesses remained in configuration control and
procedural usage.
The previously established organizational structure
impaired effective oversight of Keowee by nuclear operations. Following the
loss of offsite power event of October 1992, Keowee was reorganized, and
programs for operator standards and training were developed.
3
Performance in the radiological protection area was superior. The ALARA
program remained strong. The water chemistry and the environmental and
effluent monitoring programs were effectively implemented. The organization
was stable, and the radiological training program was good. Deficiencies were
identified with radioactive material labeling, area posting and adherence to
radiological control area access procedures.
Preventive and predictive maintenance programs were effectively developed and
implemented. These, along with management efforts to reduce existing backlogs
of work requests and temporary modifications, improved plant equipment
performance. Inadequate controls over maintenance and surveillance activities
contributed to several operational events which included reactor trips and the
October 1992 Loss of Offsite Power event.
Management commitment to the emergency response organization was evident as
the program remained strong. The response team was aggressively exercised
with numerous drills and challenging scenarios. Emergency facility equipment
was well maintained, and a siren system upgrade was fully implemented.
The security program was well managed and supported. Personnel were
effectively trained and knowledgeable of duties and responsibilities.
Initiatives were taken to review fully all operability aspects of a support
facility in order to provide appropriate security measures. Discrepancies
were conservatively documented and addressed. Improvement was noted late in
the assessment period with closed circuit television reliability.
Engineering provided good support for plant modifications, outages and
maintenance. Engineering personnel were knowledgeable and demonstrated a high
degree of ownership over their respective systems. Weaknesses existed in
resolving emergent issues and with system flow model calculations.
Performance in the operator requalification program declined from the previous
assessment period due to weaknesses in examination content and evaluator
techniques.
In the area of Safety Assessment/Quality Verification, performance was
inconsistent. Management was thorough and conservative when addressing
issues recognized as clearly safety significant and licensing submittals.
Corrective actions to improve shutdown risk and command and control of
operating evolutions were effective. A questioning attitude towards suspect
test results was not always evident, and management was slow to recognize the
need for increased oversight of Keowee operations.
4
Overview
Performance ratings assigned for the last rating period and the current period
are shown below.
Rating Last Period
Rating This Period
Functional Area
8/01/90- 2/01/92
2/02/92 - 5/01/93
Plant Operations
2
2
Radiological Controls
1
1
Maintenance/Surveillance
2
2
1
1
Security
1
1
Engineering/Technical
Support
2
2
Safety Assessment/
Quality Verification
2
2
III.
CRITERIA
The evaluation criteria which were used to assess each functional area are
described in detail in NRC Manual Chapter MC-0516, which can be found in the
Public Document Room files. Therefore, these criteria are not repeated here,
but will be presented in detail at the public meeting to be held with licensee
management on July 28, 1993.
IV. PERFORMANCE ANALYSIS
A.
Plant Operations
1.
Analysis
This functional area addresses the control and performance of activities
directly related to operation of the facility.
During the previous SALP assessment, weak or deficient operator
attention and control of evolutions during outage conditions was
identified.
During this assessment period, command and control of
operations activities improved particularly during shutdown conditions.
Configuration control errors and mispositioned equipment events
continued to occur. Procedural inadequacies, usage weakness and
inattention to detail contributed to several operational events.
Although improvement was achieved in the area of command and control
over licensed activities, there were occasions which demonstrated that
continued efforts are needed. In one case a procedure review was
inadequate when the task was inappropriately delegated. On another
occasion, operators permitted maintenance activities during low power
physics testing, which resulted in an inadvertent cooldown.
5
Operator response to transients and upset conditions was good. Prompt
action by operators prevented over-pressurization of the quench tank
during a system misalignment. Several transients requiring operator
action were handled effectively. Operators generally demonstrated
excellent knowledge of plant systems and processes. Fundamental
watchstanding practices improved from last assessment period. Shift
turnovers were thorough. Preshift meetings and mid-shift Operations
Department update meetings provided effective communications to both
operations personnel and other plant support groups.
Log keeping was
adequate, but amplifying details regarding evolutions were inconsistent.
Shift staffing exceeded Technical Specification requirements without the
need of excessive overtime. Operators properly used Abnormal Procedures
and Emergency Operating Procedures when required.
Operators were not required to have extensive knowledge of Keowee
operations. This became evident during the loss of offsite power event
in October 1992. The operators' response to and recovery from this
event was complicated by the lack of appropriate procedural guidance and
overall complexity of the various electrical power system interactions.
Adequate standards had not been established for Keowee operator
performance, duties, responsibilities and knowledge levels. Keowee
operations and management structure was subsequently reorganized to
report to Oconee Nuclear Operations Department.
Performance standards
for Keowee operations were established and implemented towards the end
of this assessment period. Also, some limited training of Oconee
operators on Keowee systems was initiated late in this assessment
period.
Configuration control and procedural adherence exhibited weaknesses that
represented a continuation of problems identified during the last SALP
period. Mispositioned equipment incidents continued to occur during
this evaluation period. Failure to follow approved procedures occurred
in several instances. In some cases procedural requirements and
policies were not clearly understood by personnel.
Procedural steps
were inappropriately marked "Not Applicable" (NA) without a thorough
review and resulted in a violation of Low Temperature Over-pressure
Protection requirements and an inadvertent draining of a portion of the
main feedwater system. Guidance on marking steps NA was implemented
midway in the period and some improvements were noted.
Other examples
included the use of the wrong unit's procedure to calculate an estimated
critical position and a failure to follow a procedure that resulted in
misplaced fuel assemblies during refueling. In one instance, an
Abnormal Procedure for restoring offsite power was considered
inadequate.
Both operators and supervisory-personnel exhibited a conservative
approach to technical issues. The Operations Support Group was
instrumental throughout the period in providing both technical and
administrative support to the control room. Work control screening,
outage scheduling and review, and procedure review and revision were
also effectively performed by this group. The Operations Support Group
was staffed primarily with licensed senior reactor operators (SROs) and
reactor operators (ROs). The experience level of both control room
personnel and the Operations Support Group were considered very high.
6
Management continued to work toward the "black board" concept and
improvement was noted by a reduction in the number of lit annunciators
and nuisance alarms. Plant equipment labeling efforts have reduced the
instances of wrong unit or wrong equipment events. Control room
drawings were maintained legible, however, changes resulting from minor
modifications were not always promptly reflected.
Operator attention and control of evolutions during shutdown conditions
improved from the previous assessment period. Management implemented
changes to control room supervisory functions, and defined operator
duties during shutdown conditions. These changes were in response to
several significant events in the previous evaluation period. Control
room decorum and professionalism improved. More formal communications
resulted in a decrease in the number of events. The duties and
responsibilities of the Operator at the Controls were revised to allow
concentration on plant status and evolutions in progress.
Administrative duties and support activities were assigned to other
personnel. These changes were effective and contributed to improved
performance during shutdown activities.
One Severity Level 3 Violation and nine Severity Level 4 Violations were
identified.
2.
Performance Rating
Category: 2
3.
Recommendations
The Board noted that problems associated with inadequate procedures and
failure to follow procedures continued from the previous SALP period.
Management corrective actions to address this weakness have not been
fully effective. A broad review of procedural usage should be
undertaken to identify the underlying causes.
B.
Radiological Controls
1.
Analysis
This functional area addresses those activities related to radiation
safety, radiological effluent control and monitoring and
primary/secondary chemistry control.
The licensee continued to maintain a stable and well-qualified radiation
protection staff with no significant changes made to the licensee's
radiological controls organization. The licensee's training program
remained sufficient during the period with program enhancements that
included instructions to plant workers and the revisions to 10 CFR Part
20, as well as the implementation of an Electronic Dose Capture System
and its interface with digital alarming dosimeters (DADs).
Early in the
assessment period, continuing training was not being provided for
contract health physics (HP) technicians. The licensee corrected this
by adding training modules focusing on refresher HP theory and practices
and providing additional training to the contract HP technicians.
7
The licensee's program to maintain overall occupational external
exposure as low as reasonably achievable (ALARA)
remained very good.
The collective dose for 1992 was 217 person-rem per unit. The
collective dose in 1993 to the end of the SALP period was 24 person-rem
per unit. During the assessment period, the licensee initiated and
completed replacement of the letdown piping and "J" leg drains from the
steam generators in Units 1 and 3. Replacing this highly radioactive
piping with new piping, thereby reducing high dose rates in the
containment basement areas, was a significant ALARA initiative.
The internal exposure controls, i.e., contamination control, the
respiratory protection, and the bioassay program, were effectively
implemented to control exposure.
No exposures exceeded regulatory
limits.
Licensee performance in the contamination control area continued to be
effective in ensuring that contaminated floor space and personnel
contamination events were maintained below established goals and were
trending down. Contaminated space was typically controlled to less than
seven percent of the radiologically controlled area (RCA).
Personnel
contamination events did not result in any skin doses or intakes greater
than regulatory limits.
During the assessment period, repetitive problems were identified with
radioactive material control practices.
Specifically, the NRC
identified: (1) recurring instances of radioactive material in the RCA
not being properly labeled as such, and (2) recurring instances of areas
in the RCA containing radioactive material not being properly posted.
As a result of the licensee's investigation of a possible skin dose
overexposure to a radwaste operator, the licensee found that the worker
rarely used the Electronic Dose Capture System to log into the RCA of
the plant.
Further investigation revealed that approximately 20 percent
of personnel working in the RCA were not logged in any radiation work
permit (RWP).
This indicated less than fully effective adherence to
procedures and control of work being conducted in the RCA.
During the assessment period, the licensee's audit program was effective
in identifying radiological control program deficiencies.
However, the
effectiveness of the audit program was reduced because corrective
actions to findings were not properly implemented.
Specifically, of 23
problem identification reports reviewed, 17 had no corrective actions
assigned for deficiencies identified, including several which were
nearly a year old.
Furthermore, out of 47 radiological deficiencies
reviewed, all but one were assigned the lowest priority for correction.
Typical issues not resolved included procedural inadequacies, non-ALARA
work practices, and miscellaneous dosimetry problems.
The licensee's performance with regard to maintaining low levels of
radiation doses from effluents was good. The whole body doses were less
than one millirem/year each from the liquid effluents and from the
gaseous effluents released during 1992.
Those doses were a small
percentage of their respective limits.
Compared to 1991, larger volumes
of liquid radwaste, with higher radionuclide concentrations, were
processed through the liquid radwaste treatment systems during 1992.
8
Although the amount of activity released increased slightly, a small
decrease in the total body dose from liquid effluents for 1992 was
achieved by a reduction of the Cs-137 concentration in the effluent. By
processing laundry waste water through powdered resin before release,
the Cs-137 concentration in the effluent was significantly reduced.
There was one unplanned release during 1992 which occurred when
approximately 2000 gallons of slightly contaminated water from the Low
Pressure Service Water System were inadvertently discharged from the
Unit 2 Low Pressure Injection Cooler to Lake Keowee. No release limits
were exceeded during that event.
Effluent radiation monitor performance was mixed. A longstanding
problem with the Low Pressure Service Water (LPSW) monitors was
corrected and the monitors for Units 1 and 2 were returned to service
during the assessment period. System modifications were required to
correct insufficient sample flow from all portions of the LPSW system.
The modification for the Unit 3 system was completed during the previous
assessment period. Late in the assessment period there were two monitors
that were inoperable for several days before the licensee detected that
they were not functioning properly. Weaknesses were identified with the
licensee's corrective actions for restoring the monitors to an operable
status.
The licensee's environmental monitoring program was effectively
implemented. The program results for 1992 indicated that there was no
significant radiological impact on the health and safety of the general
public resulting from plant operations. Dose estimates calculated from
environmental monitoring program data were in reasonable agreement with
dose estimates calculated from effluent release data and were well
within 40 CFR 190 dose limits. The licensee's performance in the
Environmental Protection Agency's interlaboratory crosscheck program
indicated that an effective quality assurance program had been
maintained for analysis of environmental samples.
The parameters required to be monitored as part of the water chemistry
control program were maintained well below their technical specification
(TS) limits. The program also included provisions for implementing,
with few exceptions, industry guidelines for PWR primary and secondary
water chemistry. The activity of reactor coolant was also maintained
well within the TS limits. The activity was slightly higher in the Unit
3 coolant than in Units 1 and 2 coolant due to residual contamination
from leaking fuel in previous fuel cycles. The licensee has since
implemented a policy of reloading fuel with zero defects with regard to
leaking fuel.
There were no transportation incidents involving the licensee's
shipments of radioactive material during the assessment period. The
program was effectively implemented and provided for preparation and
shipment of radioactive material pursuant to the Department of
Transportation's regulations.
9
Five Severity Level 4 Violations were identified.
2.
Performance Rating
Category: 1
3.
Recommendations
None
C.
Maintenance/Surveillance
1.
Analysis
This functional area addresses those activities related to equipment
condition, maintenance, and surveillance testing. In addition to the
routine inspections in this area, an Electrical Distribution System
Functional Inspection (EDSFI) was conducted during this assessment
period.
The licensee's performance in the maintenance/surveillance functional
area was inconsistent throughout the assessment period. Predictive
maintenance and equipment monitoring was aggressively pursued and was
effective whereas weaknesses were noted in areas such as procedural
adherence, documentation of problems during troubleshooting and repairs,
and maintenance/surveillance induced reactor trips and transients.
The licensee continued to focus efforts on preventative maintenance.
The thermography program introduced during the previous SALP period was
effective in identifying potentially significant maintenance problems
prior to failure and was effective in identifying leaking valves.
Management efforts were effective in significantly reducing the
maintenance work request backlog. The backlog was maintained at levels
which were better than management expectations. This contributed to
improved equipment reliability as only one reactor trip from power was
caused directly by equipment failure. Improved controls and efforts to
reduce temporary modifications have also been successful.
The maintenance department was well staffed with experienced and
knowledgeable personnel. The use of vendors and contractors was
controlled with most maintenance support performed by Duke Power
individuals. Plant material condition and routine housekeeping was
adequate.
During this period, significant operational problems were attributable
to poor maintenance controls. A loss of offsite power event and reactor
trip occurred in October 1992 due to maintenance activities conducted in
the 230 kilovolt switching station control power system. Three other
reactor trips from power occurred during maintenance activities. These
were due to problems during troubleshooting or repair activities and use
of a wrong wiring diagram. Although three refueling outages were
conducted and adequately managed, three unit shutdowns were required
during the period due to inadequately performed maintenance.
10
Problems with independent verification, undocumented work activities and
other poor maintenance practices continued to occur during the period.
Examples include an inadvertent reactor protection system channel
actuation due to performing a surveillance on the wrong unit, improper
wire terminations that were "verified" by two technicians and a Quality
Control inspector, an undocumented activity involving lifting leads and
an Emergency Feedwater Actuation due to poor scaffolding controls.
Surveillance activities caused a unit runback and testing on the wrong
unit caused a plant trip.
The test program for the Keowee Hydrostation did not adequately
demonstrate the ability of the system to perform its design function. A
periodic test had not been performed on the Keowee units to supply power
through the overhead path. Additionally relays required to isolate
portions of the switchyard and to transfer Keowee auxiliary power to an
alternate source were not fully tested. Also, as discussed Section
IV.F. (Engineering/Technical Support), LPSW testing had not been
adequately performed to validate flow model calculations until the NRC
pointed out errors in the model.
In other areas, several inadequate
surveillance procedures were identified during the period including one
The licensee's inservice inspection (ISI) program was effectively
implemented during this inspection period.
ISI non-destructive
examinations were conservatively performed.
The procedures, examination
techniques, and documentation of results were good. Personnel were
knowledgeable in their areas of responsibility. Some problems were
identified involving the failure to document and resolve welding
discrepancies identified by the vendor on ASME Code relief valves and an
untimely and inadequate relief request from postmodification hydrostatic
testing.
Seven Severity Level 4 Violations were identified.
2.
Performance Rating
Category: 2
3.
Recommendations
A significant number of plant transients were attributed to inadequate
maintenance or surveillance activities. Some of these were related to
procedural problems and work controls. A broad review of procedures,
similar to that mentioned in the Operations functional area is
recommended.
11
D.
1.
Analysis
This functional area addresses activities related to the execution of
the Emergency Plan and its implementing procedures, including licensee
performance during emergency exercises and actual events, interactions
between onsite and offsite emergency response organizations during
emergency exercises and actual events, and support and training of
onsite and offsite emergency response personnel.
Management support and involvement in the emergency preparedness (EP)
program was evidenced by the numerous drills conducted and the emergency
facility and equipment improvements made during the assessment period.
The licensee continued to administer an aggressive schedule of EP
training drills, creating challenges for the emergency response
organization (ERO) that exceeded the training requirements of the
Emergency Plan. These drills (two of which were conducted during off
hours) included annual participation by each of the five Operations
shifts in simulator-driven exercises involving the full ERO. This
approach, combined with formal classroom training, appeared to be an
effective way of maintaining organizational readiness for responding to
an emergency.
The onsite emergency preparedness staff was qualified and continued to
provide comprehensive emergency preparedness training. Offsite support
agency training for fire, ambulance, rescue, hospital, and local law
enforcement agencies was conducted in accordance with commitments in the
Emergency Plan and agreement letters with assisting agencies.
During the annual exercise in August 1992, the licensee demonstrated its
capability to provide for the health and safety of the public by
effectively implementing the Emergency Plan in response to the simulated
accident scenario. The scenario appropriately challenged the licensee's
ERO, and included full participation by the NRC. The licensee
demonstrated the ability to identify emergency conditions, to make
correct classifications in accordance with Emergency Plan implementing
procedures, to take appropriate measures to mitigate the adverse
consequences of degrading plant conditions, and to recommended
appropriate protective actions for the public. The emergency response
facilities were activated fully within the required time periods. The
timely activation and capable functioning of the Emergency Operations
Facility constituted an exercise strength. An exercise weakness was
identified for failure of the Joint Information Center to quantify or
put into perspective, for the general public, a radiological release
which occurred as a component of the scenario.
The licensee maintained emergency facilities, equipment, instrumentation
and supplies in a state of readiness with thorough equipment
inventories, surveillances, and functional tests. Just prior to the
beginning of the assessment period, the licensee fully implemented an
upgrade of the offsite siren system through the addition of a
computerized feedback capability for monitoring each siren's operation
during any mode of testing or actual activation. This resulted in very
12
high siren availability (approximately 99 percent) during 1992, with the
feedback system successfully identifying siren operability problems for
prompt corrective action.
The 1991 corporate reorganization necessitated major EP program changes
which were implemented during the assessment period.
Most of the EP
program responsibilities previously held by the corporate staff were
transferred to the site. Concurrent with this transfer of
responsibility was the relocation of many emergency response personnel
to the site. Some organizational functions were also shifted from the
Emergency Operations Facility to the Technical Support Center. However,
the totality of the functions performed did not change with the
reorganization, and adequate emergency response capabilities were
maintained.
During this assessment period, the licensee's Emergency Plan was
activated twice at the Notification of Unusual Event level.
Each of the
events was properly classified, and notifications to State and local
governments and the NRC were made in accordance with applicable
requirements.
One Severity Level 5 Violation was identified.
2.
Performance Rating
Category: 1
3.
Recommendations
None
E.
Security
1.
Analysis
This functional area addresses those safeguards activities related to
the protection provided to the station's safety related vital equipment,
and the assurance that individuals authorized station access are fit for
duty.
The licensee's safeguards program was well managed at the site level as
evidenced by the professionalism and effectiveness of its proprietary
security force.
Officers were well trained, knowledgeable of their
duties and responsibilities, well versed in their procedures, and
adequately equipped. Shifts were appropriately staffed.
The licensee conducted effective quality assurance audits which were
thorough and complete.
Corrective actions for the audit findings were
timely and appropriate.
As noted in previous SALP assessments, the licensee's closed circuit
television system, used to assess protected area barrier alarms,
continued to be non-operational in several zones. Several television
13
monitors located inside the alarm stations were frequently out of
service. Thus, the licensee continued to use compensatory measures to
meet its Plan commitments during the period. Toward the end of the SALP
period, camera assessment system reliability had greatly improved.
The licensee completed an engineering evaluation of certain non-vital
piping which, given various operational modes and valve lineups, could
be important to safety and therefore should be protected. This
licensee's initiative in conducting this review was well coordinated
with the NRC and adequate compensatory measures have been implemented
where necessary.
With respect to other elements of the safeguards program, access
controls and alarm station operations were appropriate, barriers and
alarms were maintained as required, lighting was sufficient, and (except
as noted earlier regarding cameras) maintenance and compensatory
measures were adequate.
During this SALP period, the licensee identified several security events
involving inadequate communications. A failure by the Control Room
operators to notify the security shift that a facility important to
safety was not operable resulted in the failure to institute timely
compensatory actions. A failure by Human Resources personnel to notify
the security shift of a positive drug test resulted in an unauthorized
access to the Station. Also identified by the licensee was its failure
to conduct daily communications tests as committed to in its Security
Plan. These were appropriately documented in the Safeguards Event Log.
In addition, the NRC identified several Plan inaccuracies relative to
the Turbine Building security barrier. The licensee took appropriate
corrective actions for the aforementioned events.
The licensee has clarified its generic Corporate Procedure for Reporting
Safeguards Events to ensure that NRC reporting criteria is met. This
has resulted in an overall increase in reporting events in the
Safeguards Logs.
No violations were identified.
2.
Performance Rating
Category: 1
3.
Recommendations
None
14
F.
Engineering/Technical Support
1.
Analysis
This functional area addresses activities associated with the design of
plant modifications and of technical support for operations, outages,
maintenance, licensed operator training and requalification.
Engineering support was strongest in support of plant operations and
planned outages. Weaknesses were evident in the response to emergent
issues not directly related to operability and in corrective actions.
Licensed operator training improved, but some weakening of the
requalification program was evident. The staffing of the engineering
organizations was satisfactory.
Engineering support for plant modifications was adequate. The quality
and technical content of temporary and minor modifications was generally
good. Examples included the addition of Vent Valve ICCW-422, relocation
of IC-850 and IC-852, and snubber additions on main feedwater and
emergency feedwater piping. There were also instances found of
inadequate design calculations and reviews, although some of the
inadequacies occurred before this assessment period. Examples included
previous and current Low Pressure Service Water (LPSW) flow model
calculations used to justify operability of the system. After the NRC
identified the errors, the licensee corrected them and then tested the
LPSW to verify operability. The tests demonstrated that the LPSW
systems were degraded in that excessive flow through the low pressure
injection coolers could be achieved under certain design basis
conditions and that LPSW flow through the reactor building cooling units
could be significantly below the assumed accident condition flow rate.
The flow testing conducted on Unit 3 also identified that the system was
degraded due to a mispositioned valve. Single failure vulnerabilities
were also identified in the design basis documentation previously
conducted.
The licensee's engineering and technical support have been responsive to
station needs. Examples include identification and prompt communication
to the NRC of the need to change a prior commitment relating to post
accident boron dilution flow monitoring, modifications to correct
degraded control voltage to the "S" and "E" breakers, corrective action
for inadequate Keowee auxiliary breaker closing power, and modifications
to the Standby Shutdown Facility makeup pump accumulators. Engineering
has generally provided prompt and well-founded solutions to short-term,
operational problems. The response to other issues in which immediate
operability was not an issue has not been quick or as thorough.
Examples include problems with Keowee X-relays, numerous LPSW issues
(raised by the NRC), and a revised response to NRC Bulletin 88-04
concerning the deadheading of LPSW pumps. Also, the planning for the
replacement of switchboard batteries did not identify potential problems
with operating a battery charger without a connected battery. This
resulted in a loss of offsite power and a reactor trip to Unit 2.
System engineers assumed "ownership' of their assigned systems and
15
actively participated in the resolution of problems. Component
engineering provided good support to maintenance.
Engineering support for the resolution of other emerging issues, not
identified as requiring immediate corrective action, was sometimes
deficient. Examples of problems noted included: (1) the failure to
perform a safety evaluation for a temporary modification (installation
of an electrical jumper on radiation monitor interlock to Valve 2LWD-2);
(2) the use of incorrect design drawings in the completion of a plant
modification (resulting in a reactor trip); (3) an inadequate
engineering evaluation of the operability of a letdown storage tank
check valve; (4) failure to take prompt and adequate corrective actions
for low indicated service water flow through the 3B Low Pressure
Injection (LPI) Coolers; and (5) failure to correct the MG-6 testing
deficiency after identification during Keowee Unit 2 testing.
An Electrical Distribution System Functional Inspection revealed
problems in testing, design analyses, and design basis documentation.
Similar problems were also found in the Oconee emergency AC power
source. These problems resulted in part from the lack of a thorough
understanding of the design basis of the site's electrical distribution
system.
Operator training was effective. Improvements were noted in the initial
training of licensed operators.
This good performance was indicated by
the successful completion of all seven candidates nominated for licenses
in January 1993.
The candidates exhibited good communications and
interactions during their simulator examinations, but had a generic
weakness in radiation protection.
The previously noted problems with
simulator fidelity to the plant have been rectified.
The performance of
requalification was satisfactory.
During the June 1992 requalification
examination, five of six crews and 22 of 24 operators passed.
Weaknesses noted included the content and construction of the written
test and poor or improper cuing during the job performance measures.
This was in contrast to the strong performance of facility evaluators
during the previous assessment period.
Two Severity Level 4 Violations were identified.
2.
Performance Rating
Category: 2
3.
Board Recommendations
None
16
G.
Safety Assessment/Quality Verification
1.
Analysis
This functional area addresses those activities related to the
licensee's implementation of safety policies related to license
amendments, exemptions and relief requests; responses to Generic
Letters, Bulletins and Information Notices; resolution of safety issues;
reviews of plant modifications performed under 10 CFR 50.59; safety
review committee activities; and the use of feedback from self
assessment programs and activities.
Management performance in the area of safety assessment and quality
assurance was inconsistent. Efforts to correct weaknesses in command
and control were effective, however many repetitive problems continued
in the area of procedural compliance by personnel.
Prompt followup to
deficiencies was not always evident. Licensing documentation and
submittals were generally very good.
Management implemented several corrective actions to improve the
operation of the station in areas previously identified by the NRC as
weak or deficient.
Improved performance was noted in shutdown risk and
control room command and control. Initiatives to improve the conduct of
outage activities and the reduction in shutdown risk vulnerability were
noteworthy. Of particular note was the reduction in control room
distractions, efforts to more fully inform employees of outage
activities, and an independent safety assessment of the outage schedule.
The Nuclear Safety Review Board was objective and thorough in its review
of operations and problems at Oconee. Management was responsive to the
comments and recommendations from the Board.
In the area of Keowee operations and design, management was slow to
recognize the need for corrective action to address previously
identified NRC concerns and weak areas. In September 1992 a management
meeting was held at NRC request to discuss these issues. The licensee
indicated that while some changes to procedures were appropriate, major
operational, organizational and procedural changes were not necessary.
However, in October 1992, a loss of off site power event occurred and
followup inspections identified significant weaknesses in these areas.
It should be noted that the licensee's Significant Event Investigation
Team, dispatched to site to review the event, was effective in
determining root causes, safety implications and provided
recommendations for corrective action.
Following these inspections, a
comprehensive Emergency Power Management Plan was developed. This plan
was intended to substantially improve the overall operation and
maintenance of the Keowee facility. An organizational change was also
made to incorporate the Keowee station under Oconee station line
management.
At the conclusion of this assessment period the
effectiveness of these changes remained under evaluation.
Issues which the licensee recognized as clearly safety significant were
normally resolved aggressively. Actions were conservative and thorough,
and involved early interaction with the staff. Examples included 100
per cent steam generator tube inspection, corrective action for degraded
17
control voltage for "E" and "S" breakers and corrective actions related
to the emergency electrical system after the Unit 2 Loss of Power event.
At times, the failure to further probe into questionable indications led
to untimely identification of adverse conditions. Examples included the
failure to investigate abnormal LPSW flow during valve testing and
failure to promptly investigate abnormal position indication on a Keowee
breaker. Management efforts to address the large number of operator
errors and procedure violations have not been fully effective as they
continued to occur in a number of areas in the plant.
A significant improvement was noted in the quality and timeliness of
Inservice Inspection and Testing relief requests since the last
evaluation period. Most amendments and relief requests were processed
without the need for additional clarifying information or supplements to
the original submittal. When additional information was required, the
licensee was very responsive in providing the requested information
promptly.
The licensee provided responses to NRC requests within the time frame
requested or provided written notification if circumstances prevented
meeting the requested schedule. These responses were generally clear,
precise, and sufficient. Examples include responses to Generic Letter 91-11, Vital Instrument Busses and Tie Breakers, Generic Letter 88-20,
Independent Plant Examinations, and Generic Letter 87-02, Seismic
Qualification of Mechanical and Electrical Equipment in Operating
Plants. However, in one instance, an inadequate response to Bulletin
88-04, Safety Related Pump Loss, was not corrected until NRC requested a
revised response.
Licensee Event Reports (LERs) in most cases were timely and well
written. One report, LER 269/92-12, concerning various problems with
the Unit 1/2 LPSW system, was submitted late.
Two Severity Level 3 Violations and two Severity Level 4 Violations were
identified.
2.
Performance Rating
Category:
2
3.
Recommendations
None
V.
SUPPORTING DATA AND SUMMARIES
A.
Licensee Activities
A major reorganization was announced in November 1991, including relocating
Design Engineering to the site. Implementation of the reorganization was
completed in July 1992. Additional management changes during this assessment
period included the April 1, 1993, reassignment of Mr. R. L. Sweigart, former
18
Superintendent Operations, to Superintendent Work Control and Mr. G. E.
Rothenberger, former Superintendent Work Control, to Superintendent Operation.
There were three refueling outages during this assessment period. Refueling
outages were completed in March 1992 for Unit 2, September 1992 for Unit 3,
and January 1993 for Unit 1. These outages were satisfactorily completed with
no major problems. However, the Unit 3 refueling outage required extensive
decontamination activities due to the contamination which occurred inside
Unit 3 Containment following the November 23,
1991, break of a 3/4-inch tubing
connector on the Reactor Coolant System. During the Unit 1 refueling outage,
a larger than normal number of degraded steam generator tubes were identified
which were required to be plugged. This was attributed primarily to revised
tube plugging criteria.
In September 1992, the licensee determined that both trains of the Units' 1
and 2 LPI system were inoperable. The cooling water flow of the LPSW system
through the LPI heat exchangers were found to exceed the manufacturer's
specifications. The power level for both units was reduced to approximately
10 percent and modifications were made to reduce the flow through the heat
exchangers to meet the manufacturer's specifications.
On October 19,
1992, during maintenance activities, a loss of off site power
occurred for Unit 2 which was followed by a subsequent loss of the Keowee
Hydro Station.
Since this event, the licensee has placed the Keowee Hydro
Station under the Oconee management and has implemented a number of procedure
changes to improve the reliability of the emergency power supply for the
Oconee Station.
B.
Direct Inspection and Review Activities
In addition to the 36 routine NRC inspections and two initial and three
requalification examinations performed at the Oconee facility, the following
three special inspections were conducted:
December 9, 1991
February 21, 1992
Shutdown Risk Inspection
October 20 - 28, 1992
Augmented Inspection Team (AIT) Loss of
Off-site AC Power Supply
January 25 - March 5, 1993
Electrical Distribution System Functional
Inspection (EDSFI)
C.
Escalated Enforcement Activities
1.
Orders
None
2.
Civil Penalties (CP)
Two Severity Level III problem violations (IR 91-32/EA 91-167) were
issued on February 3, 1992, involving ten specific violations related to
the degradation of the decay heat removal event of September 7, 1991 and
19
the over-pressurization of the LPI system piping on September 19-20,
1991. ($125,000) Although both of these events occurred during the
previous assessment period, the violations were issued during this
assessment period on February 3, 1992.
A Severity Level III violation (EA 92-211) was issued on December 28,
1992, and involved the failure to take adequate corrective action to
resolve a reduced Low Pressure Service Water System flow condition
through the Unit 3B Low Pressure Injection system cooler. ($100,000)
The licensee requested mitigation of the civil penalty. Subsequent to
this assessment period, an order to pay was issued which the licensee
complied with.
D.
Management Conferences
February 5, 1992: A meeting was held in Region II for Duke to discuss
the items identified during the Design Basis Documentation Program
evaluation of the Oconee electrical systems and the corrective actions
initiated on the identified problems.
June 24, 1992: A meeting was held in Region II for Duke to discuss the
shutdown risk procedures to be implemented for future Oconee refueling
outages. Also, discussed were Duke's Problem Investigation Program,
procedure adherence and configuration control programs at Oconee.
July 17, 1992:
An enforcement conference was held in Region II to
discuss the circumstances associated with the May 8, 1992, Unit 1
reactor trip in which one of the two required Emergency Feedwater System
flow paths was not operable and the operation of Unit 1 from May 11
through 24, 1992, with only one of the two Emergency Feedwater System
flow paths operable.
September 17, 1992: A meeting was held at the Oconee facility to
discuss the operation, management and maintenance of the Keowee Hydro
Station.
November 24, 1992:
An open enforcement conference was held in Region II
to discuss the circumstances associated with the mispositioned valve in
the Unit 3 Low Pressure Service Water System.
March 29, 1993: A meeting was held at NRC Headquarters to discuss
electrical issues at Oconee.
Several additional meetings were held with Duke Power throughout the
assessment period to discuss a variety of other subjects including
licensing activities, safety initiatives, Oconee's self-assessment, the
Emergency Data System and the development status of a Babcox and Wilcox
digital module for use in the reactor protection system.
E.
Confirmation of Action Letters (CAL)
Following the October 19, 1992, Unit 2 reactor trip and loss of power
event, a CAL was issued to address the cause of the event. On October
26, 1992, a conference call was held and the licensee discussed
enhancements to be made to the Keowee Hydro Station and Keowee
20
operations.
These commitments were documented in a letter to the NRC
dated October 27, 1992.
F.
Reactor Trips/Unplanned Shutdowns
Seven automatic reactor trips occurred. Five of these were attributed
to maintenance/surveillance activities, one to equipment failure and one
to operator error. These trips are as follows:
Unit 1
May 7, 1992: The unit experienced a reactor/turbine trip from 100
percent power due to a connector coming loose on the generator exciter
field. (Maintenance/Surveillance)
May 8, 1992:
The unit tripped from 14 percent following a turbine trip
due to the loss of suction to the "lA main feedwater pump which was
caused by pressure swings while lowering hotwell level.
(Operations)
Unit 2
October 19, 1992: The unit tripped from 100 percent power on the loss
of off-site power which occurred during switchyard battery modification
work when a battery charger was placed in service without a connected
battery. (Maintenance/Surveillance)
Unit 3
February 27, 1992: The unit tripped from 100 percent power following a
turbine trip due to human error. A technician was testing the loss of
generator stator cooling on Unit 2 which was shutdown in a refueling
outage but inadvertently performed the test on Unit 3.
(Maintenance/Surveillance)
June 24, 1992: A turbine/reactor trip occurred from 100 percent power
while technicians were replacing low pressure service water
instrumentation. A fuse blew in the Integrated Control System when an
incorrectly wired card was installed. This caused a momentary loss of
power to the steam generator water level instrumentation which resulted
in a turbine/reactor trip.
(Maintenance/Surveillance)
September 29, 1992: The unit tripped from 73 percent power due to low
reactor coolant system pressure from a defective Group 5 control rod
drive programmer. (Equipment Failure)
January 26, 1993: A turbine/reactor trip from 100 percent power
occurred due to low main feedwater pump discharge pressure which was
inadvertently caused by a technician during trouble shooting activities.
(Maintenance/Surveillance)
21
G.
Review of Licensee Event Reports (LERs)
During the assessment period, 30 LERs were analyzed. The distribution
of these events by cause as determined by the NRC staff was as follows:
Cause
Total
Unit 1 Common Unit 2 Unit 3
Component Failure
5
2
3
Design
9
8
1
Construction/Fabrication
1
1
Installation
Other
2
1
1
Personnel
- Operating Activity
6
4
1
1
- Maintenance Activity
3
1
2
- Test/Calibration Activity
2
1
1
- Other
2
1
1
TOTALS
30
8
15
2
5
Notes:
1.
With regard to the area of personnel, the NIRC
considers lack of procedures, inadequate procedures,
and erroneous procedures to be classified as personnel
error.
2.
The other category is comprised of LERs where there
was a spurious signal or a totally unknown cause.
3.
One Special Report was submitted. Also, two LERs were
submitted but were later rescinded. These reports are
not included in the above tabulation.
4.
The above information was derived from a review of
LERs performed by the NRC staff and may not completely
coincide with the licensee's cause assignments.
H.
Licensing Activities
During the rating period, approximately 175 active licensing actions
were submitted for the three Oconee units of which 97 were completed.
There were 33 licensing amendment requests of which 24 were completed.
22
I.
Enforcement Activity
No. of Deviations and Violations in Each Functional Area:
V
IV III
II
I
Plant Operations
-
9
1
Radiological Controls
-
5
Maintenance/Surveillance
-
7
Security
Engineering/Technical
-
2
Support
Safety Assessment/Quality
-
2
2
-
Verification
TOTALS
1
25
3
-
NOTE:
Two of the Severity Level 3 violations and the Severity Level 5
violation were identified during the previous assessment period, but
reports were not issued until this assessment period.