ML15118A277

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Insp Repts 50-269/97-15,50-270/97-15 & 50-287/97-15 on 971019-1115.Violations Noted.Major Areas Inspected:Aspects of Licensee Operation,Engineering,Maint & Plant Support
ML15118A277
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 12/15/1997
From: Ogle C
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML15118A275 List:
References
50-269-97-15, 50-270-97-15, 50-287-97-15, NUDOCS 9712310358
Download: ML15118A277 (54)


See also: IR 05000269/1997015

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos:

50-269, 50-210

50-287, 72-04

License 'Nos:

DPR-38 DPR-47, -DPR-55 SNM-2503

Report No:

50-269/97-15, 50-270/97-15, 50-287/97-15

Licensee:

Duke Energy Corporation

Facility:

Oconee Nuclear Station Unis 1 2. and 3

Location:

7812B Rochester Highway

Seneca, SC 29672

Dates:

October 19 - November 15, 1997

Inspectors:

M. Scott. Senior Resident Inspector

S. Freeman, Resident Inspector

E. Christnot, Resident Inspector

D. Billings. Resident Inspector

B. Crowley, Regional Inspector (Section M1.4)

J. Blake, Regional Inspector, Review at Eddy Current

Analysis Center (Sections M1.6 and M2.2)

N. Economos, Regional Inspector (Section M2.3)

R. Franovich, Resident Inspector, Catawba (Section M1.7)

R. Moore, Regional Inspector (Sections E2.1, E3.1. and E8.1)

N. Merriweather, Regional Inspector (Sections E2.1, E3.1.

and E7.1)

D. Forbes, Regional Inspector (Sections R1 through R7)

B. Miller, Regional Inspector (Sections F1 through F7)

Approved by:

C. Ogle, Chief, Projects Branch 1

Division of Reactor Projects

Enclosure 2

9712310358 971215

PDR ADOCK 05000269

Q

PDR

EXECUTIVE SUMMARY

Oconee Nuclear Station, Units 1. 2. and 3

NRC Inspection Report 50-269/97-15,

50-270/97-15, and 50-287/97-15

This integrated inspection included aspects of licensee operations,

engineering, maintenance, and plant support. The report covers a four-week

period of resident inspection, and the results of announced inspections.by

region-based inspectors.

Operations

In general, the conduct of operations was professional and safety

conscious.

(Section 01.1)_

Refuelfi gactivities were completed in a professional and conservative

manner. The use of, the reactor engineer on the refueling bridge in the

reactor building, the use of an extra licensed operator in the spent

fuel pool area during refueling, and the new level of licensee safety

conscious overview were strengths. (Section 01.2)

The licensees power reduction and replacement of a degrading Unit 2 main

seal oil pump was proactive and performed without incident.

(Section 02.1)

  • .

The inspectors concluded that the licensee's program and preparations

for cold weather were good. (Section 02.2)

Maintenance

The inspectors concluded that general maintenance activities were

completed thoroughly and professionally. (Section M1.1)

During the period, the licensee searched for and found a missing piece

from the 1A1 Reactor Coolant Pump impeller. During the search, the

licensee found other reactor vessel related pieces that had been missing

since 1981. The licensee was generating an evaluation on the vessel

related piece that would remain in place. Video inspection of the

Unit 1 reactor coolant pumps had been performed and the licensee was

evaluating continued operations of the three pumps with observed

impeller degradation for an additional fuel cycle. (Section M1.2)

Strong management oversight, good communications, and sound coordination

by engineering and maintenance resulted in an error free recovery of a

-- *broken

MARB stopple plug from the low pressure service water system.

(Section M1.3)

The Failure Investigation Process team was aggressively pursuing the

root cause for the failure of the MARB0 plugging tool. All maintenance

Enclosure 2

2

and inspection activities observed for installation of the 24-inch MARBO

plug were performed in a conscientious manner by qualified personnel in

accordance with detailed procedures. Welding and non-destructive

examination activities observed and reviewed were performed in

accordance with the applicable code and procedure requirements..

(Section M1.4)

The failure by maintenance personnel to complete a Technical

Specification required surveillance on low pressure injection flow

instruments resulted in a violation. (Section M1.5)

The licensee's process for the evaluation of steam generator eddy

current .data was being conducted in accordance with current industry

guidelines and expectations. (Section M1.6)

The practice of obtaining anoil sample from the Unit 2 turbine driven

emergency feedwater pump without it running was a weakness in the oil

sampling methodology. A request by operations for a procedure to govern

the realignment of the pump's steam supply was seen as a conservative

measure to protect the steam header piping and structural supports from

possible water and steam hammers. (Section M1.7)

Assembly of low pressure service water valves with the wrong parts

resulted in an Unresolved Item concerning parts identification. (Section

M2.1)

The condition of the Oconee once-through-steam-generators has seen

additional licensee attention through Babcock & Wilcox Owners Group

sponsored tube pulls in each unit, and the contract with Dominion

Engineering Incorporated to do an independent review of the Oconee steam

generator program. (Section M2.2)

The failures of mechanical feedwater piping connections to the Unit 1B

steam generator were not being identified and trended as repeat

failures. (Section M2.2)

The licensee implemented repairs in once-through-steam-generator 1B

tubes in a conservative manner, following administrative controls and

applicable controlling procedures. Technical support provided good

guidance and oversight while the activity was in progress. (Section

M2.3)

Engineering

Based on a review of engineering activities, engineering support to

operations and maintenance was adequate. (Section E2.1)

Enclosure 2

3

Design.control for a Unit 1 low pressure service water modifications was

good. The 10 CFR 50.59 evaluations were detailed and thorough.

(Section E3.1)

The engineering self-assessments performed in,1997 were effectivin

identifying and assuring correction of deficiencies in engineering

performance. (Section E7.1)

The failure to revise the Updated Final Safety Analysis Report to

reflect different fuel enrichments since 1994 was identified as a.

violation. :The discrepancy had been previously identified, but went

uncorrected. (Section E8.3)

Plant Support

Based on. observations and procedural reviews, the inspectors determined

the licensee was effectively maintaining controls for radioactive waste

and waste processing- One unresolved item was identified to determine

monitoring requirements for radiological work in two onsite buildings.

The licensee's initiative to improve resin sluice processing systems to

maintain exposures As Low As Reasonably Achievable and to improve

environmental controls for resin sluicing was viewed as a strength.

(Section R1.1)

It was concluded that the licensee's water chemistry control program for

monitoring primary and secondary water quality had been effectively

implemented, for those parameters reviewed, in accordance with the

Technical Specification requirements and the Station Chemistry Manual

for Pressurized Water Reactor water chemistry. (Section R1.2)

The inspectors determined that the licensee had effectively implemented

a program for shipping radioactive materials required by NRC and

Department of Transportation regulations. (Section R1.3)

It was concluded that the meteorological instrumentation had been

adequately maintained and that the meteorological monitoring program had

been effectively implemented. (Section R2.1)

The inspectors determined that the licensee was performing Quality

Assurance audits and effectively assessing the radiation protection

program as required by 10 CFR Part 20.1101. The inspectors also

determined that the licensee was completing corrective actions in a

timely manner. (Section R7.1)

The licensee's fire protection staff demonstrated an aggressive attitude

in the identification and correction of fire protection deficiencies.

(Section F1.1)

Enclosure 2

4

Three non-cited violations were identified for the licensee's failure to

meet the fire protection operability requirements for three required

fire protection features. (Section F1.1)

The low number of inoperable or degraded fire protection components, in

conjunction with the good material condition of the fire protection

components and fire brigade equipment. indicated appropriate emphasis

had been placed on the maintenance and operability of the fire

protection equipment and components. (Section F2.1)

Adequate surveillance and test procedures were provided for the fire

protection systems and features, and implementation of the procedures

was effective. (Section F2.2)

The fire barrier penetration seals were' functionak However, the

licensee had implemented a project to provide documentation to identify

the design specification and bounding test criteria applicable to each

fire barrier penetration. (Section F2.3)

In general. fire protection program implementing procedures were well

written and met the licensee's commitments to the NRC requirements.

Procedure implementation for the control of ignition sources and

transient combustibles was good. Overall, general housekeeping was

satisfactory. (Section F3.1)

A violation was identified involving the failure to provide fire

fighting strategies for all plant areas which contained safety-related

equipment or presented an exposure hazard to safety-related components.

(Section F3.1)

The fire brigade organization and training met the requirements of the

site procedures. The use of the fire brigade safety officer position

during fire emergencies was identified as a program strength. (Section

F5.1)

Fire brigade performance during a drill conducted during this inspection

period was mixed. Subsequent brigade performance after resolution of

drill identified deficiencies was satisfactory. (Section F5.1)

The 1995 audit and assessment of the facility's fire protection program

were comprehensive and appropriate corrective action was promptly taken

to resolve identified issues.

(Section F7.1)

Enclosure 2

Report Details

Summary of Plant Status

Unit 1 began and ended the period in a scheduled refueling outage. Major

outage work completed included the replacement of the 1A1 reactor coolant

pump, inspection of the other reactor coolant pump impellers, and low pressure

service water system modifications.

Unit 2 began the period at 100 percent power and decreased to 56 percent power

on November 6. to repair the generator main seal oil pump motor. The unit

returned to 100 percent power on November 7. and remained at 100 percent power

for the. rest of the period.

Unit 3 began and ended the period at 100 percent power.

Review of Updated Final Safety Analysis Report (UFSAR) Commitments

While performing inspections discussed in this report, the inspectors reviewed

the applicable portions of the UFSAR that related to the areas inspected.

Except for the issues discussed in Sections E8.3 and F. the inspectors

verified that the UFSAR wording was consistent with the observed plant

practices, procedures, and parameters.

I. Operations

01.

Conduct of Operations

01.1 General Comments (71707)

Using Inspection Procedure 71707, the inspectors conducted frequent

reviews of ongoing plant operations. In general the conduct of

operations was professional and safety-conscious: specific events and

noteworthy observations are detailed in the sections below.

01.2 Unit 1 Refueling Activities

a. Inspection Scope (71707)

The inspectors observed portions of the defueling and refueling

activities for Unit 1.

b. Observations and Findings

The inspectors observed control room, spent fuel pool (SFP), and reactor

building (RB) activities by operations personnel. The activities were

conducted in a professional manner with emphasis on attention to detail,

conservative judgement, and timeliness. During the initial checkout of

  • equipment,

problems with the RB manipulator were identified and

resolved. The licensee made enhancements in refueling activities

Enclosure 2

2

including the use of a reactor engineer on the refueling bridge in the

RB and the-use of an extra licensed operator in the SFP area during

refueling. Licensee management also articulated a new level of licensee

safety conscious overview for refueling. The inspector observed that

operators in the control room were aware of the movement of each fuel

assembly by number and monitored appropriate nuclear instrumentation.

c.

Conclusions

Refueling activities were completed in a professional and conservative

manner. The use of the reactor engineer :on the refueling bridge in the

RB, the use of an extra licensed operator in the SFP -area during

refueling, and the new level of licensee safety conscious overview were

strengths.

02

Operational Status of Facilities and Equipment

02.1 Unit 2 Power Reduction for Seal Oil Motor Replacement

a. Inspection Scope (71707, 62707)

The inspectors attended several meetings and observed work in progress

as the icensee reduced power to replace the Unit 2 seal oil pump motor.

b. Observations and Findings

On November 6 and 7, 1997, the licensee evaluated a degrading bearing on

the main seal oil pump motor. Routine vibration monitoring detected

higher than expected vibration levels on the motor, which worsened over

November 6. After a management meeting on the afternoon of November 6,

the licensee reduced power on Unit 2 to 56 percent. As the down power

continued, maintenance personnel removed the equivalent motor from

Unit 1, which was shut down for refueling, and overhauled it by

replacing the bearings. The switch between seal oil skid pumps was

safely performed and the main pump motor was changed out using the

overhauled pump from Unit 1. The unit was restored to full power on

November 7.

c. Conclusions

The licensee's power reduction and replacement of a degrading Unit 2

main seal oil pump were proactive and performed without incident.

Enclosure 2

3

02.2 Cold Weather Preparations

a. Inspection Scope (71714)

The inspectors reviewed the licensee's program for cold weather

preparations and the status of freeze protection equipment.

b. Observations and Findings

The inspectors documented in Inspection Report (IR)

50-269,270.287/96-16

previous worklorderseand discrepancies involved with freeze protection

equipment. The IR indicated the following: a corporate audit was

performed to formalize a freeze protection program for all three nuclear

sites; Problem Identification Process (PIP) report 096-0639 was

initiated to address concerns raised -by the audit: and procedure

upgrades that are planned or being evaluated by site .management were

discussed. In addition, the IR also identified three susceptible areas:

(1)

the borated water storage tank (BWST) level indication: (2)

the,.

elevated water storage tank (EWST) level indication: and (3)

the cooling

water to the condenser circulating water (CCW) pumps.

The inspectors reviewed PIP 096-0639 and observed that several

corrective actions were initiated. Among the items affected by the

corrective actions were:

plant equipment used for freeze protection,

such as heat trace and heaters: areas of the plant and equipment

requiring cold weather protection, including Keowee; and administrative

control, inspection, and maintenance procedures required to implement a

freeze protection program.

The inspectors reviewed applicable procedures and observed the

following:

IP/0/B/1606/009, Preventive Maintenance and Operational Check of

Freeze Protection, Revision 0, provided a method for inspecting,

cleaning, and performing an operational check of freeze protection

equipment.

Nuclear System Directive (NSD) 317. Freeze Protection Program,

Revision 1, provided the guidelines and requirements to ensure

that sub-freezing conditions do not impair the safe and efficient

operation of nuclear power plant equipment.

MP/0/B/3007/059, Plant Heater - Testing, Revision 1, provided

--

guidance for the testing of plant heaters.

The inspectors observed and reviewed work activities involved with

procedure IP/0/B/1606/009. These activities were performed on freeze

Enclosure 2

4

protection equipment associated with the BWST., EWST. and the CCW cooling

water supply.

c. Conclusions

.

The inspectors concluded that the licensee's preparations and program

for cold weather were good.

03

Operations Procedures and Documentation

03.1 Failure to Perform Instrument Surveillance on the Inadequate Core

Cooling Monitor (ICCM)

a. Inspection Scope (71707)

On October 29, 1997:, during the performance of PT/3/A/0600/01. Periodic

Instrument Surveillance, operations identified that Technical

Specification (TS) requirements had not been met due to the operator aid

computer (OAC) subcooling monitor calculation being non-conservative.

.

b. Observations and Findings

TS 1.5.3 requires an instrument channel check to verify acceptable

instrument performance by comparison to an independent channel measuring

the same variable. To meet this requirement for the ICCM,

PT/3/A/0600/01 required the operator compare the ICCM subcooling values

with the OAC subcooling values. PIP 097-1394 was initiated on April 30,

1997. to document a problem with the coefficients used in the OAC

subcooling monitor calculation. The operators had been initialing the

step in PT/3/A/0600/01 with a note stating that the OAC points were out

of service. This did not meet the intent of the TS surveillance. As an

interim corrective action, engineering developed a procedure to allow

operators to perform a manual calculation using control room instrument

values to verify the subcooling margin. The inspectors will continue to

follow the licensee's evaluation through Licensee Event Report (LER) 50

287/97-04 and the associated PIP 097-3784 concerning TS surveillance

requirements.

II.

Maintenance

M1

Conduct of Maintenance

M1.1 General Comments

a. Inspection Scope (62707, 61726)

The inspectors observed all or portions of the following maintenance

activities:

Enclosure 2

5

TT/1/A/0400/28

Standby Shutdown Facility Reactor Coolant Makeup

Pump Flow Distribution

WO 9709228601.

Unit 1 Perform Video Inspection of Reactor Core

Support Area

PT/1/A/0610/01J

Emergency Power Switching Logic Functional Test

IP/0/B/1606/009

Preventive Maintenance and Operational Check of

Freeze Protection

MP/0/A/3007/059

Plant Heater - Testing

IP/0/A/3000/015

125 Volt Direct Current 230 Kilovolt Switchyard

Battery Service Test and Annual Surveillance

WO 97062732-1

Perform Annual Switchyard Battery Surveillance

b. Observations and Findings

The inspectors found the work performed under these activities to be

professional and thorough. A

work observed was performed with the

work package present and in use. Technicians were experienced and

knowledgeable of their assigned tasks. The inspectors frequently

observed supervisors and system engineers monitoring job progress.

Quality control personnel were present when required by procedure. When

applicable, appropriate radiation control measures were in place.

c. Conclusion

The inspectors concluded that the maintenance activities listed above

were completed thoroughly and professionally.

M1.2 Unit 1 Reactor Coolant Pump (RCP) Impellers and Loose Parts in Reactor

Coolant System (RCS)

a. Scope of Inspection (62707, 37551)

As discussed in IR 50-269,270,287/97-014. Section M1.9. the licensee

found a piece of the vane missing from the 1A1 RCP impeller. The

inspectors followed the licensee's actions and were informed that these

actions will be captured in PIP 097-4012.

b. Observations and Findings

The licensee inspected the RCS and reactor vessel to the maximum extent

practicable to locate the missing piece. The piece was found in the

  • -bottom of the reactor vessel. Additionally, the licensee found a

Enclosure 2

6

thermal shield bolt head and a core support assembly guide block which

were previously reported missing. These parts were discussed in LER 50

269/81-11. The LER included supporting documentation from the RCS

vendor Babcock & Wilcox, to justify continued operation. The impeller

piece and bolt were removed. The guide block was firmly wedged between

the core support assembly rib section and the incore guide support

plate. The licensee was in the process of completing an evaluation of

the observed conditions at the end of the report period. To date, the

licensee's retrieval actions have been adequate.

The licensee inspected the impellers on the three remaining RCPs for

potential cavitation induced erosion. The licensee contracted with a

vendor for an articulated, high-resolution camera that could completely

inspect the details of the impellers, particularly the back side of each

impeller vane. All three impellers had indications of erosion damage

that was to be documented in PIP 097-4012. The inspectors viewed the

video tape made during the inspection and discussed the findings with

the licensee and other NRC personnel. The licensee and the pump vendor

were evaluating the damage at the end of the inspection period.

M1.3 Low Pressure Service Water (LPSW) MARBO Stopple Pluq Failure

a. Inspection Scope (62707,40500)

The inspectors reviewed documents and drawings, interviewed personnel.

and observed activities associated with the failure and subsequent

recovery of a 36-inch MARBO stopple plug in the LPSW piping.

b. Observations and Findings

On October 17. 1997, while removing the 36-inch MARBO stopple plug, a

loud knock was heard at the stopple machine and a water and oil mixture

was observed coming from the view port. Licensee personnel quickly

reacted to contain the oil and prevent a oil discharge to the lake.

Vendor personnel, with licensee approval, continued to attempt to remove

the stopple plug and close the 36-inch isolation valve. The valve

closed smoothly to the halfway point and stopped. The valve was cycled

and again an attempt was made to remove the stopple plug. The valve

would not close fully and the coordinator entered the stopple plug loss

contingency plan. A Failure Investigation Program (FIP) team was

formulated to determine the cause and PIP 097-3621 was generated.

On October 20, 1997, a video was completed by the vendor of the inside

of the valve. The video showed that the stopple plug was separated from

the ram assembly used to position the plug. The break was located at

the point where the ram met the pivot plate. The contingency plan to

remove the broken stopple plug was discussed with management. A

-modification package. TN/1/A/11029/00/01M. for performance of another

Enclosure 2

7

MARB0 plug to allow recovery of the 36-inch plug was completed on

October 23. 1997. The new 24-inch MARB0 connection was completed on

October 26, 1997. The 24-inch MARB0 plug was installed on October 27,

1997. with the subsequent recovery of the 36-inch MARB0 plug and the

removal of the 24-inch MARBO plug on October 28. 1997.

The broken 36-inch MARB0 plug was sent to Southwestern Research

Institute for metallurgical analysis.

c. Conclusions

Strong management oversight, good communications, and sound coordination

by engineering.and maintenance resulted in an error free recovery of a

broken MARBO stopple plug from the LPSW system.

M1.4 LPSW Piping Modification

a. Inspection Scope (62700)

The inspectors observed ongoing work activities relative to installation

of a stopple (MARBO) plug in a 24-inch diameter LPSW pipe. See

paragraph M1.3 for further discussion on roblems encountered with a 36

inch MARB0 plug upstream of the 24-inch plug, which necessitated the

installation of the 24-inch plug.

b. Observations and Findings

As discussed in paragraph M1.3. while removing a stopple (MARBO) plug

from the 36-inch LPSW line downstream of the C LPSW pump, the plugging

machine hydraulic ram broke before the plugging head was completely

removed from the split tee fitting and sandwich valve. The sandwich

valve could not be closed to isolate the plugging machine from the

system. Therefore, another MAR80 plug was installed in the 24-inch line

downstream of the 36-inch plug to isolate the plug so that the broken

ram and plugging machine could be removed from the 36-inch line. The

inspectors observed the following activities relative to investigation

of the cause of the ram failure for the 36-inch plug and installation of

the 24-inch plug:

Failure Investigation

A failure investigation had been initiated by a FIP team. The

inspectors discussed the failure with the FIP team leader and reviewed

-

the preliminary results of the investigation. The ram broke near the

end-cap weld at the attachment to the plugging head. Based on pictures

taken with a remote camera prior to removal of the plugging machine, the

FIP team stated that the failure appeared to be fatigue in nature. A

Enclosure 2

8

metallurgical analysis was planned after removal of the plugging

machine.

Installation of 24-inch Pluq

The 24-inch MARBO plug was installed by Minor Modification Project

Numbers ONOE-11028 and ONOE-11029. The applicable code for fabrication

and installation of the :split tee -was USAStandard Code for Pressure

Piping B31.1, July 1967 Edition. In addition to reviewing the

modificationlpackages and various in-process work procedures and

documents-, the inspectors observed and reviewed the following welding

and:inspection activities:

In-process welding was observed for Weld 6 (flange to split tee)

on Isometric Drawing 1-LPS-570. In addition, in-process final

visual and magnetic particle examinations were observed for the

weld.

Final weld surfaces were visually inspected on the split-tee Welds

2. 3. 4 and 5 on Isometric Drawing 1OLPS-570.

For Welds 2. 3. 4, 5, and 6 on Isometric Drawing 1OLPS-570, weld

process control sheets and weld material issue records were

reviewed; and welder qualification, welding material

certification, and nondestructive examination/quality control

(NDE/QC) inspector qualifications were verified.

c. Conclusions

The FIP team was aggressively pursuing the root cause for the failure of

the MARBO plugging tool. All maintenance and inspection activities

observed for installation of the 24-inch MARBO plug were performed in a

conscientious manner by qualified personnel in accordance with detailed

procedures. Welding and NDE activities observed and reviewed were

performed in accordance with the applicable code and procedure

requirements.

M1.5 Low Pressure Injection Flow Instrument Surveillance Interval Exceeded

a. Inspection Scope (62707)

The inspectors interviewed licensee personnel and reviewed documents and

work orders associated with the low pressure injection (LPI) system flow

instrumentation surveillances.

Enclosure 2

9

b. Observations and Findings

On October 7, 1997, the inspectors requested documentation to verify the

testing of the LPI system. On October 10. 1997, with Unit l.in a

refueling outage. Unit 2 at 100 percent power, and Unit 3 in hot s

shutdown, the licensee identi'fied that the surveillance for the.flow

transmitters had not been completed on Unit 1 since January 26, 1995,

and onUnit 3-since February1

1995.

The procedure containing this calibration had been performed onUnit 1.

and 3, but only the calibration of the differential pressure indicator

had:been performed. The complete surveillance, including the flow

transmitters, had been completed for Unit 2 on July 21, 1997. Following

identification of the omission, the complete calibration procedure was

completed for Unit 1 on October 11. 1997, and for Unit 3 on October 10.

1997, with no discrepancies noted.,.

An investigation was initiated to verify no other omissions of TS

surveillances. PIP 7-097-3465 and LER 50-269/97-09 were generated. The

investigation revealed no other missed TS surveillances. The root cause

was identified as failure to follow procedure. The surveillance had

been scheduled, but the technicians did not perform the procedure as

specified. Failure to complete required TS surveillances is a violation

(VIO) of TS requirements and is identified as VIO 50-269,287/97-15-01:

Failure to Complete Required TS Surveillances on LPI Flow Instruments.

c. Conclusions

The failure by maintenance personnel to complete a Technical

Specification required surveillance on low pressure injection flow

instruments resulted in a violation.

M1.6 Steam Generator (SG) Eddy Current Examinations

a. Inspection Scope (50002)

The inspector reviewed the licensee's program and procedures for eddy

current analysis, and observed the activities of the resolution analyst

team for the Oconee 1 outage, which commenced on September 18. 1997.

The procedures reviewed were as follows:

NDE-701, Multifrequency Eddy Current Examination of Steam

Generator Tubing at McGuire, Catawba. and Oconee Nuclear Stations.

Revision 3, Field Change 97-09. September 9. 1997.

NDE-703, Evaluation of Eddy Current Data for Steam Generator

Tubing, Revision 5, Field Change 97-10. September 9, 1997.

Enclosure 2

01

10.

  • :NDE-707, Multifrequency Eddy Current Examination of Non-ferrous

Tubing. Sleeves and Plugs Using a Motorized Rotating Coil Probe.

Revislon 3,.Field Change 97-13, September 16, 1997.

NDE-708, Evaluation of Eddy Current Data for Non-ferrous Tubing,

Sleeves and Plugs Using a Motorized Rotating Coil Probe,

Revision 3, Field Change 97-11, September 9, 1997.

Data Management/System Administration Guidelines - Oconee Unit 1

End.oftCycle-17JEOC-17). Revision 0, September 17. 1997.

Eddy Current Guidelines', Oconee Nuclear Station, Unit 1, EOC-17.

Revision 0, September 17, 1997.

The licehsee's eddy current data evaluation facility is located on the

grounds of the McGuire Nuclear Station, near Charlotte, North Carolina

(NC).

For the Oconee Unit 1 SG eddy current examinations the primary

analysts were working in Lynchburg, Virginia (VA)- and the secondary and

resolution analysts were working at the licensee's facility.

O b. Observations and Findings

As required by the licensee's program, eddy current data were being

analyzed by two independent groups of analysts, referred to as the

primary and secondary analysts, with differences between the two

resolved by independent resolution analysts. The primary analysts for

this Oconee Unit 1 outage were working at the Framatome facility in

Lynchburg, VA, and the secondary and resolution analysts were working at

the licensee's facility at the McGuire site.

The inspector observed the activities of the resolution analysts during

resolution of differences between the results of primary and secondary

analyses. As a part of the resolution process, the analysts were able

to bring past inspection data on the screen for direct comparison of

previous signals with the current data.

c. Conclusions

The licensee's process for the evaluation of steam generator eddy

current data was being conducted in accordance with current industry

guidelines and expectations.

Enclosure 2

M1.7 Maintenance on Turbine-Driven Emergency Feedwater Pump (TDEFWP) Turbine

Steam Supply Valves

a. Inspection Scope (61726)

A Unit .2

TDEFWP .surveillance test was scheduled to be performed on

October 28, 1997, and maintenance activities were scheduled to be

performed the same Iday before pump testing.

The inspectors reviewed

surveillance test procedure PT/2/A/0600/12, Turbine Driven Emergency

Feedwater Pump Test,:Revision 53: reviewed maintenance procedure

MP/0/A/1840/040, Pumps-Motors-Miscellaneous Components-Lubrication-Oil

Sampling-Oil Change, Revision 6; reviewed operating procedure

OP/2/A/1106/06. Enclosure 3.13, Isolation and Return of Main Steam

Supply to the TDEFWP, written October 30..1997: discussed the

maintenance and testing activities with operations, maintenance, work

control and engineering personnel: observed various maintenance and

testing activities; reviewed the UFSAR, design basis documentation, and

associated system drawings; and observed pre-job briefings and various

operator actions in support of maintenance and testing activities in'the

control room.,

b. Observations and Findings

At 5:32 a.m., on October 28, 1997, the Unit 2 TDEFWP was removed from

service for planned maintenance in preparation for a quarterly TDEFWP

surveillance test. Maintenance activities included analysis of the

TDEFWP bearing oil and repair of 2SD-307. a drain valve in the main

steam supply line to the pump turbine. In preparation for the repairs

to the steam line drain valve, main steam to the TDEFWP was isolated;

auxiliary steam from the Unit 3 main steam line was available.

Oil samples were obtained from the inboard and outboard pump bearing

housings and analyzed; the results indicated that the sample was

contaminated with suspended solids. A second sample was obtained and

met acceptance criteria: the pump was declared operable (the remaining

steam drain valve repair did not require that the TDEFWP be inoperable

since auxiliary steam was available and at the required pressure).

To ensure that the pump bearings were unaffected, engineering personnel

proposed running the pump to demonstrate that the bearings were not

damaged and confirm the results of the second oil sample. Operations

personnel had already returned the TDEFW pump to service under the

assumption that, since the second sample results met acceptance

criteria, the pump was operable. Although the pump run proposed by the

engineering personnel was a conservative measure to demonstrate pump

operability, a miscommunication between the organizations resulted in a

premature return to service of the TDEFWP. Station PIP 097-3797 was

Enclosure 2

12

initiated to address the discrepant oil samples and subsequent decision

to test the pump bearings.

On October 29. 1997, a performance test of the TDEFWP-was-performed to

demonstrate that the pump bearings were functional. The inspectors

observed the pump start and run: no discrepancies were identified..

The inspectors questioned a maintenance supervisor why the initial oil

sample was contaminated. Maintenance technicians initially had drawn

the oil samples .througha.

small piece of plastic tubing by inserting one

end of the tubing into the bearing housing and using a hand-pump to

transfer the sample from the housing through the plastic tube and into a

sample bottle on the other end of the tube. Apparently, the end of

plastic tubing:had traveled along the inner wall of the bearing housing

and disturbed a film of debris on the wall surface, which was drawn into

the sample bottle. To obtain.the second sample, maintenance technicians

drained the oil from the bearing housings into a container. The oil was

stirred, and a sample was taken from the mixed medium.

The inspectors determined that the initial oil sample had not been

obtained after the pump had been run to ensure that the sample

represented a well-mixed, homogenous population of oil. The inspectors

reviewed maintenance procedure MP/0/A/1840/040. Pumps-Motors

Miscellaneous Components-Lubrication-Oil Sampling-Oil Change, Revision

6. and determined that the procedure did not require that the pump

operate prior to sampling to ensure adequate mixing of the oil.

The

inspectors discussed sampling methodology with a maintenance supervisor,

who indicated that sometimes pumps are run prior to oil sampling, but

not always. The inspectors expressed concern that the practice of not

running a pump, or other piece of equipment with components requiring

oil lubrication, prior to obtaining an oil sample could fail to reveal

contaminants in the sample and, thereby, contaminants in the population.

The inspectors considered the practice a weakness in the oil sampling

methodology.

The inspectors verified that the TDEFWP was restored to operable status

within the time allowed by TS. The inspectors also observed portions of

the maintenance to repair the steam leak on 2SD-307, which was completed

on October 29, 1997. Operations personnel raised concerns with

water/steam hammers associated with returning the isolated portion of

main steam supply piping to service. Although this realignment had been

performed in the past, it was not proceduralized and controlled to

minimize the risk of water/steam hammers. Operations requested that a

procedure be developed to govern the steam line's return to service.

The procedure. OP/2/A/1106/06. Enclosure 3.13. Isolation and Return of

Main Steam Supply to the TDEFWP. was developed on October 30, 1997. The

inspector reviewed the procedure and identified no concerns. The steam

line was returned to service without incident. The inspectors

Enclosure 2

0

13

considered the request for a procedure to govern the realignment a

conservative measure to protect the piping and structural supports.

c. Conclusions

The inspectors considered the practiceiof obtaining .an oil sample,

without running the associated equipment a weakness in the oil sampling

methodology. The request for a procedure to govern the realignment of

the Unit 2 TDEFWP steam supply was a conservative measure to protect the

piping and structural supports.

M2

Maintenance and Material Condition of Facilities and-Equipment

M2.1 Wronq ServiceWater Valve Parts

a. Scope of Inspection (61726)

During the inspection period, the licensee was rebuilding several valves

in the LPSW system. The inspectors followed activities on two valves.

O b. Observations and Findings

During re-assembly of valve 1LPSW-565. supply to reactor building

auxiliary coolers, maintenance personnel observed that the new trunnion

parts could not be installed properly. The trunnions connect the bottom

and top of the ball valve to the operating shaft; thus allowing ball

rotation/movement. The new trunnions were approximately 1/4-inch taller

than the removed trunnions. PIP 097-4025 was initiated on November 11,

1997, the day of discovery.

Investigation indicated that the eight-inch trunnion parts intended for

1LPSW-565 had been installed into 1LPSW-4, the 1A LPI cooler outlet

isolation valve, which was a ten-inch valve. This valve had been

returned to service. The 1A train of LPI was declared inoperable and

the 1B LPI train was available for service as required in Selected

Licensee Commitment 16.5.6. Tentative licensee review indicated that

the parts had been marked incorrectly and not detected prior to

dispersal from the licensee's supply.

The eight-inch parts were removed from 1LPSW-4, examined and re

certified. The 10-inch parts were re-certified and installed in 1LPSW-4

and the eight-inch parts inspected and installed in 1LPSW-565. Both

valves were tested and returned to service. As of the end of this

period, the PIP and its attendant investigation were not complete.

Unresolved Item (URI) 50-269.270,287/97-15-02, Valve Parts

Identification Problem, is identified to track this issue.

Enclosure 2

14

c. Conclusions

Assembly of LPSW valves with the wrong parts resulted in an Unresolved

Item concerning parts identification.

M2.2 Once-Through-Steam-Generators (OTSGs)

a. Inspection Scope (50002)

During the week of September 8. 1997. the inspectors reviewed licensee

and contractor reports related to the material condition of the Oconee

OTSGs. The reports reviewed included the licensee's latest steam

generator maintenance, outage summary reports for each of the units: a

component .health status determination report prepared by the licensee: a

series 'of reports prepared by Dominion Engineering Incorporated (DEI)

concerning the condition of the Oconee OTSGs: and Asea Brown Boveri

Combustion Engineering test reports about eddy current and pressure

testing-of Unit 3 OTSG tubes pullediduring the last outage.

b. Observations and Findings

Licensee Outage Summary Reports

The review of outage summary reports showed the following data

concerning the number of tubes plugged during the last outage, why they

were plugged, and the total number of tubes currently plugged in each

OTSG.

Unit 1

Unit 2

Unit 3

EOC-16 (11/95)

EOC-15 (4/96)

EOC-16 (10/96)

SG 1A

SG 1B

SG 2A

SG 2B

SG 3A

SG 3B

Dings

7

5

-

-

-

Erosion/Corrosion

17

47

0

6

23

13

Groove Intergranular 2

42

119

54

51

16

Attack (IGA)

Unit 1

Unit 2

Unit 3

EOC-16 (11/95)

EOC-15 (4/96)

EOC-16 (10/96)

SG 1A

SG 1B

SG 2A

SG 2B

SG 3A

SG 3B

Wear

4

1

8

14

2

5

% Through-Wall (TW) 27

36

11

43

3

9

Sleeve

1

0

0

0

1

Enclosure 2

15

Other

7

17

7

12

9

6

IGA or Precursor

-

-

5

29

-

Groove IGA

IGA:

-

-

47

55

26

42

Lane & Wedge

-

-

2

0

-

Upper Roll

-

-

-

-

-

19

Transition

Total this Outage

65

148

199

213

115

110

Previous

334

1177

138

268

455

371

Total Plugged

399

1325

337

481

570

483

% This Outage

0.42% 0.95%

0.89% 1.37%

0.74%

0.71%

.

Total Tubes

15,531 15,531

15,531 15.531 15.459 15.531

% of Total

2.57%

8.71%

2.17%

3.10%

3.69%

3.11%

Tubes

While the data from these reports indicate that OTSG lB is in the poorer

condition (8.71% plugged), the Units 2 and 3 OTSGs had a significant

number of tubes plugged due to freespan axial indications. (The

freespan axial indications are referred to as Groove IGA and IGA in the

data set.)

The outage reports for Units 2 and 3 described tube pulls that were done

as a result of a Babcock and Wilcox Owners Group (BWOG) program to

investigate free-span cracking, originally found in the-Oconee Unit 1

OTSG. There were four full-length tubes removed from the 2A OTSG. and

three full-length and two partial-length tubes pulled from the 3A OTSG.

These tubes were in addition to the seven tubes pulled from the Oconee

Unit 1 OTSG in 1994, where the free-span cracking (IGA/IGSCC) was

initially confirmed.

Electrosleevinqm field trial

Other items of interest in the outage summary reports included the fact

that during the Unit 1 outage in November 1995, Framatome Technologies

conducted a field demonstration of the Electrosleevingm process for

electro-plating metallic Nickel on the inside surface of OTSG tubes to

-seal off existing defects and provide a barrier against further

degradation. Nine tubes that were scheduled to be plugged were selected

Enclosure 2

16

and Electrosleeves" were deposited at the first support plate. The

Electrosleevingm process was jointly developed by Framatome Technologies

and Ontario Hydro Technologies. Oconee Unit 1 was the first field

deployment of the system. The use of the process under field

conditions, including processing of the electroplating solutions as

contaminated, hazardous waste, was reported as a success. The condition

of the tube and the resulting Nickel plating were not reported, in that

the tubes were plugged after-plating.

OTSG lB Feedwater Nozzle Leakage

The inspectors noted that the Unit 1 outage summary reported that repair

work was done to remove leak-seal clamps from the flange connections

between main feedwater risers No. 1 and No. 32 and the 1B OTSG shell.

This item was of interest because'the inspectors had learned that these

same two flange connections were found to be leaking last January, while

the unit wasishut down for other reasons, and were leak-sealed again.

During the review of how the licensee was handling the repeat leakage

problems on feedwater risers No. 1 and 32. the inspectors questioned

whether these failures would be considered a functional failure under

the maintenance rule. Discussions with the engineers responsible for

administering the maintenance rule program revealed that for the

feedwater system, because it is a Class 2 system, the absence of system

leakage was not one of the fifteen listed functions monitored by the

program. After additional discussions, which included the site

Engineering Manager, the licensee decided to generate a PIP form to

document the repeat failure for trending purposes, and to question

whether system leakage should be a maintenance rule function of the

portion of the feedwater system inside the containment.

Dominion Engineering, Inc. (DEI) Reports

The inspectors reviewed the following three reports concerning the

Oconee OTSGs:

DEI-483 - Evaluation of Steam Generator Tube Damage Mechanisms

DEI-484 - Steam Generator Life Prediction Analysis

DEI-485 - Review of Chemistry and Operating Procedures

These reports, dated February 1997, were provided as an independent

analysis of the Oconee 1, 2. and 3 OTSGs. During discussions with

licensee engineering, operations, and chemistry personnel, the

inspectors learned that as a direct result of recommendations in the DEI

reports, the licensee had already implemented changes.

Enclosure 2

17

The licensee had revised operations procedure OP/1/A/1106/08. Steam

Generator Secondary Hotsoak, Fill, Drain, and Layup, Revision 35.

because DEI had concluded that'the condition of the secondary water

chemistry during startup operations was more critical to the condition

of the OTSG tubes than the water chemistry during full-power operations.

The licensee had ordered equipment, and was preparing to modify the

feedwater system for the injection of titanium oxide during'the next

refueling-outage for each unit. The addition of titanium oxide is to

provide an inhibitor in an attempt to tie up sodium hydroxide (NaOH),

especially during startups, to assist in the prevention of additional

intergranular attack (IGA) to the outside surface of the OTSG tubing.

ABB Combustion Engineering Nuclear Operations (ABB CENO) Reports

The inspectors reviewed the following reports provided to the licensee

by ABB CENO concerning tests conducted on three full-length, and two

partial-length tubes removed from the 3A OTSG:

447-PENG-TR-086, Comparison of Field and Laboratory Eddy Current

Testing (ECT) Results, Helium Leak Tests and Observations of

Oconee Unit 3 Steam Generator Tube Sections

447-PENG-TR-091, Burst Testing of Oconee 3 Steam Generator Tube

Sections

The tests reported by ABB CENO were presented in the reports in a

clinical fashion; that is,

the parameters and results of the tests were

presented without final conclusions. The conclusions concerning the

tests will be provided upon completion of the metallurgical analyses of

the tube sections. This part of the examination is still under way by

ABB CENO.

c. Conclusions

The condition of the Oconee OTSGs has seen additional licensee attention

through BWOG sponsored tube pulls in each unit, and the contract with

DEI to do an independent review of the Oconee steam generator program.

The failures of mechanical feedwater piping connections to the Unit 1B

steam generator were not being identified or trended as repeat failures.

M2.3 Repairs of Unit 1 OTSG Tubing

a. Inspection Scope (50002)

Through work observation, procedure and records review, the inspector

"-determined the adequacy of OTSG 1B tube repairs in response to eddy

Enclosure 2

18

current identified indications in the roll transition area of the upper

tube sheet (UTS).

b. Observation and Findings

Background

Eddy current inspection of OTSG lB tubes was performed during the

current outage (EOC-17). This inspection showed that certain tubes

exhibited indications at the roll transition region within the UTS and

at certain freespan locations. The UTS findications were identified as

single or multiple axial or volumetric which typically require roll

repair or plugging. In general, the subject indications were

characterized as internal diameter intergranular stress corrosion cracks

(IGSCC).

The volumetric indications were believed to be the result of

intergranular attacks (IGA). In order to investigate these indications

further, the licensee selected five tubes with representative indication

for investigation. These tube sections were pulled and sent to a

laboratory for destructive and non-destructive examinations to determine

the failure mechanism. At the time of this inspection. November 3,

1997, the licensee had not received an official report on the subject

tubes. At the completion of the eddy current examination the licensee

had identified approximately 1936 tubes in OTSG 1B that required repair.

This repair involved the re-roll of a one-inch long section of tube

below the region where tube defects were identified. The repair

established a new mechanical tube-to-tubesheet structural joint and a

new primary pressure boundary within the tube.

Observation

Through work observation. document review and discussions with the

licensee's cognizant personnel and the vendor's onsite lead engineer,

the inspector ascertained the following:

Tube re-roll repairs were being performed by Framatome

Technologies, Inc., (FTI). The work was being performed under

FTI's QA program and as such FTI was responsible for control of

equipment and processes. Representatives of Duke's Supplier

Verification Group observed the subject activity and reviewed

applicable procedures, equipment calibration records and personnel

qualification records for adequacy. The verification group found

them-to be satisfactory.

During the inspection, as of November 3. 1997. the roll repair activity

was still in progress. The inspector observed the repair of selected

tubes to verify that the applied torque to achieve the desired tube

Enclosure 2

19

expansion did not exceed established procedural limits: that post-roll

tube diameter was within established maximum and minimum limits; that

equipment was properly calibrated and performing its functions and that

personnel were properly qualified. The controlling procedure for the

repair was FTI's Document 1246068A, Revision 3 dated June 18, 1997. In

addition, the inspector reviewed FTI's two nonconformance reports

applicable to this activity.. One ofthese involved a communication

problem between the computer ahd the roll expander tool and the other

involved operator error resulting in the inadvertent repair of 13 tubes.

Corrective measures taken to prevent recurrence of these problems were

considered appropriate.

Following the close of this inspection, the inspector obtained the

following information on Oconee's Unit 1 OTSG tube repairs.

Tubes Pluqqed

1A

52 tubes were removed from service. Five were located in the lower

tubesheet (LTS).

1B

122 tubes were removed from service. Five were located in the

UTS roll transition area of interest.

Tube Pulls

1A

Five tubes were pulled from LTS. These were scheduled for

analysis.

lB

Five tubes were pulled from UTS and sent for analysis. Two of

the three samples with volumetric indications were subjected to

nondestructive and destructive examinations.

Re-Roll

1A

39 tubes were re-rolled in the UTS that will remain in service

18

Approximately 1956 tubes were re-rolled in the UTS and will remain

in service.

In addition, the inspector determined that the subject repair activity

was implemented with relatively good results in that only five re-rolled

tubes failed to meet acceptance criteria and were plugged. Also, out of

approximately 2000 tubes roll repaired, only 16 were re-rolled

- -

inadvertently.

Finally, by letter dated November 18, 1997, from W. R. McCollum, Jr., to

the Nuclear Regulatory Commission, the licensee indicated that all roll

repaired tubes in the Oconee Unit 1 OTSG B UTS region, have been

Enclosure 2

20

classified as Category C-3 as defined in Technical Specifications 4.17.3.d. Therefore all roll repaired tubes will have the new roll area

inspected during future inservice inspections.

c.

Conclusion

The licensee implemented repairs in OTSG.B tubes ofUnit Pin a

conservative manner, following administrative controls and applicable

controlling procedures. Technical support provided good guidance and

oversight during the activity.

III. Engineering

E2

Engineering Support of Facilities and Equipment

E2.1 Review of Engineering Backlog

a. Inspection Scope (37550)

The inspectors reviewed the engineering support of facilities and

equipment as demonstrated by backlogs of engineering work associated

with operator workarounds. work orders on engineering hold. PIP reports,

nuclear station modifications. minor modifications, and temporary

modifications (TMs). Applicable regulatory requirements included 10 CFR

50 Appendix B and the licensee's Quality Assurance program.

b. Observations and Findings

The inspectors noted that the overall backlog in engineering had

increased during the past year. A significant portion of the increase

was in the number of PIPs. The licensee attributed this increase to the

Unit 2 pipe rupture event that occurred in September 1996 and the

ensuing code compliance work that was performed on all 3 units. The

inspectors found that the number of PIPs open for greater than 6 months

has declined for the past 3 months to the current level of approximately

315. However, this total was still higher than that in October 1996.

The licensee tracks PIPs greater than 6 months old and has established

goals to reduce this number to 204 by the end of the year.

The inspectors reviewed the active TMs and found that 12 had been

installed for greater than 18 months. Six were installed on Unit 1,

which was in a refueling outage. Of those six on Unit 1, five were

-

-

being closed or removed during this outage. The one remaining item (TM

1188) was to be closed in the next Unit 1 end-of-cycle (1EOC18)

refueling outage which was scheduled for March 1999. The licensee

indicated that a nuclear station modification was required. Temporary

modification number 1188 was installed because the 1D3 reactor building

Enclosure 2

21

auxiliary cooling coil was leaking and closing the isolation valves both

upstream and downstream of the coil did not fully isolate the leak. The

TM installed blind inserts in the LPSW line to isolate.the 1D3 'reactor

.building auxiliary cooling coil that was leaking. The inspectors

reviewed the TM and associated 10 CFR 50.59 safety evaluation and)found

them to be acceptable. The licensee indicated that two additional TMs

greater than 18-months old were also being closed. This would leave

five TMs still open that were greater than 18 months old;., however, .none

of the remaining ones involved safety-related systems.

The inspectors-found that the Mechanical Civil Equipment Group (MCE) had

a, much larger, backlog of work orders on hold over 30 days old than those

in the other engineering groups. The inspectors discussed this with the

licensee and found that MCE considered most of these items to have a

lower priority as compared to other work items such as operator

workarounds or PIPs. The inspectors discussed the status of most of

these items with the supervisors and found that the technical basis for

these items having a lower priority appeared to be acceptable.

The inspectors found that the backlog of operator workarounds was up due

to 11 new items being added between July and October of this year. The

licensee indicated that this increase was a reflection of their ability

to better identify from the PIP database those issues that are

considered operator workarounds and was not reflective of a lack of

engineering response.

The inspectors found that 36 modifications were unscheduled or

unslotted. This issue had been identified during the licensee's

Modification Selection/Activation Process Performance Assessment SA-97

58 conducted in May 1997. The assessment included a recommendation to

management to have the large number of outstanding activated

modifications be evaluated by an independent review group to assure that

each modification can be justified. The licensee indicated that this

review was scheduled for November 1997.

c. Conclusions

Engineering support to operations and maintenance was adequate.

E3

Engineering Procedures and Documentation

E3.1 Review of Modifications

a. Inspection Scope (37550)

The inspectors reviewed the modifications to the Unit 1 LPSW system and

an unrelated electrical minor modification.

The LPSW modifications

Enclosure 2

22

review included issues identified by previously identified NRC item IFI

50-269,270,287/96-13-03 related .to service water system modification and

testing., The following modifications were reviewed:

NSM-13001/AM1, Install Minimum Flow Piping at LPSW Pumps. dated

June 17. 1997

NSM-13001/AM2,. Tie in Minimum Flow Piping to LPSW Pumps, dated

August 15, 1997

NSM-13001/CM1 Installation of Valve 2LPSW-139, dated July 30, 1997

NSM-13002, Replace 1A, lB, and.1C LPSW Impellers, dated May 28.

1997

NSM-13022, Replace Valves 1LPSW-251. -252, -254. and -256. dated

August 28. 1997

NSM-12977, Replace Valves 1LPSW-4, -5. -6,

and-15. dated

September 11, 1997

S*

ONOE-10447, Hot Taps for 14-inch and 36-inch LPSW Piping, dated

August 19. 1997

ONOE-11028, Installation of 24-inch Split Tee Fitting on LPSW

Piping, dated October 19. 1997

ONOE-11029, Perform 24-inch Hot Tap and Line Stop on LPSW Piping,

dated October 23, 1997

ONOE-8790. Analog to Digital Conversion of Reactor Protection

System (RPS) Channels A.B.C,and D Hardware, dated April 1. 1997

Applicable regulatory requirements included American National Standards

Institute (ANSI) N45.2.11-1974. Quality Assurance Requirements for the

Design of Nuclear Power Plants. 10 CFR 50.59, 10 CFR 50 Appendix B,

UFSAR, and the licensee's Quality Assurance (QA) program.

b. Observations and Findings

Design change documentation adequately identified and referenced

appropriate design inputs. Post-modification testing was adequate to

verify the function of modified equipment. In particular, the

--

modification to install the new pump impellers included adequate flow

testing to establish baseline values for Section XI testing. The

testing verified that pump capacity was essentially equal to previous

capacity and consistent with the vendor pump performance curves.

Testing was performed by the vendor to verify that the minimum flow

Enclosure 2

23

capacity (500 gallons per minute) provided by the installed

recirculation lines was adequate for at Teast,24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> of pump operation

as required by the recirculation line modification design criteria.

Severallmi.nor modifications were implemented to facilitate installation

of in-line piping stops (MARBO plugs) for isolation to replace valkes or

pump changes. Implementing procedures included contingency actions to

address potential problems anticipated during the plug replacement and

removal. Appropriate seismic analysis. was performed to facilitate

temporary hardware for plant installation. Field walkdowns demonstrated

that seismic supports were consistent with design drawings.

c. Conclusion

Design control for the Unit I LPSW modifications was good. The 10 CFR

50.59 evaluations were detailed and thorough.

E7

Quality Assurance in Engineering Activities

E7.1 Review of Engineering Self-Assessments

a. Inspection Scope (37550)

The inspectors reviewed engineering self-assessment activities that were

performed in 1997. Applicable regulatory requirements included 10 CFR

50 Appendix B. and the licensee's QA program.

b. Observations and Findings

The inspectors reviewed 13 self-assessment reports of engineering

support and design control activities that were performed in 1997 and

found them to be adequate. The assessments resulted in several findings

and recommendations being identified. The inspectors found that the

reports were clear and concise and that the findings were being tracked

by the corrective action program.

c. Conclusions

The engineering self-assessments performed in 1997 were effective in

identifying and assuring correction of deficiencies in engineering

performance.

E8

Miscellaneous Engineering Issues (92903)

E8.1 (Closed) IFI 50-269,270,287/96-09-03: Expected End-of-Cycle Heat Loads

  • This item addressed an apparent inconsistency between the UFSAR and

supporting design calculations regarding end-of-cycle SFP heat load

Enclosure 2

e

24

values associated with normal and abnormal SFP loading. The licensee

was revising the SFP heat load calculation to address anticipated

changes in fuel design and cycle lengths at the time the item was

identified. The IFI was identified to track the licensee's verification

that the UFSAR specified heat load values for the two conditions bounded

the calculated values.

The inspectors reviewed OSC-4998, Units 1 and 2 SFP Heatup Rate

Calculation, Revision 7. and UFSAR Sections 9.1.3.1.1 and 9.1.3.3.1,

which were revised December 31, 1996, to verify resolution of this item.

The,,calculation determined the bounding heat load conditions for the

normal _and abnormal SFP loading using fuel burn-up assumptions

appropriate to the anticipated core design and cycle length. The normal

case heat load was within the previously specified UFSAR value. The

abnormal heat load for future anticipated fuel conditions slightly

exceeded the previously specified UFSAR value for this case. Both

values were within the capacity of the SFP cooling system specified in

the UFSAR. The December 31, 1996, UFSAR revision deleted the specific

heat load values and core off load descriptions from the UFSAR. The

revision additionally clarified that the abnormal case (full core

offload) was the routine condition during refueling outages.. The

inspector concluded this item was adequately resolved.

E8.2 (Clsd BaR_

52

7-03 Revision 0

0 and 1: Post LOCA Boron Dilution

Design Basis Not met Due to Deficient Design Analysis

(Closed) URI 50-269,270287/97-01-06: Boron Dilution Flow Path

Inoperability

This issue involved the identification of a possible failure of the Post

LOCA Boron Dilution flowpaths though LP-1 and LP-2. In Revision 0, the

licensee identified through an engineering evaluation of Generic Letter 96-06, that LP-1, LP-2. LP-103, and LP-104 could be inoperable due to

thermal over pressurization. This would remove both active boron

dilution flow paths from service. Following questioning by the

inspectors, the licensee realized they had conservatively neglected the

impact of the holes drilled in the upstream disk of LP-1 and the bonnet

reliefs on LP-2. These modifications had been made in 1985, 1986, and

1987. Therefore, the active path through LP-1 and LP-2 were operable

from the time these modifications were completed to the present. LP-103

and LP-104 were inoperable from initial installation until the recent

outages when a void was introduced between the valves. Engineering will

perform an evaluation to determine if any other actions are recommended

to provide additional margin for LP-1 and LP-2. This evaluation is

captured inaPIP 0-097-0279: therefore, this LER and URI are closed.

Enclosure 2

25

E8.3 (Closed) URI 50-269,270,287/97-12-02: Fuel Load UFSAR Statements

This URI concerned a discrepancy between the UFSAR and two existing

refueling 10 CFR 59.59 evaluations. Specifically, UFSAR

Section 4.3.3.1.4 stated in part that "Each fuel rod is identified by an

enrichment code, and the-design of the reactor is such that only dhe

enrichment is used per assembly." However, the licensee had installed.

fuel in Unit 2 in 1994 and Unit 3 in 1997 that contained different

enrichment (axial blankets) without indicating this discrepancy in their

safety evaluations or clarifying the statements in the UFSAR that

described one enrichment fuel.

This was an oversight, but was not

recognized until after the refuelings had occurred. Once recognized in

PIP 0-097-0448 (February 3, 1997), it was not addressed in the next

UFSAR update issued in July 1997 nor were the 10 CFR 50.59 evaluations

changed. PIP 0-097-2511, initiated on August 13. 1997, by an

independent site review, brought the matter to a head and an

investigation was performed * The 10 CFR 50.59 evaluation for the

pending Unit 1 refueling had yet to be, completed at the time that PIP 0

097-2511 was initiated. The licensee subsequently completed their

evaluation of the problem with the issuance of Root Cause Investigation

for PIP 0-097-2511, dated September 23, 1997. The inspectors discussed

the problem with the licensee and observed the corrective action scheme.

The investigation revealed that several causes had prevented a proper

10 CFR 50.59 review for a fuel change or the accomplishment of UFSAR

updates to reflect actual fuel configurations. The investigation

summary root causes were primarily attributed to misjudgement in the

level of UFSAR review for the 10 CFR 50.59 evaluation and misjudgement

in the level of validation and verification needed to assure corrective

action commitments such as a PIP were adequately documented and

responsibilities were assigned.

Based on the above, the inspector concluded that the failure to revise

the UFSAR to reflect the different fuel enrichments was a violation of

10 CFR 50.71(e). This is identified as VIO 50-270.287/97-15-09:

Failure to Update the UFSAR Regarding Fuel Enrichment.

IV.

Plant Support Areas

R1

Radiological Protection and Chemistry Controls

R1.1 Tour of Radiological Protected Areas

a. Inspection Scope (84750)

The inspectors reviewed implementation of selected elements of the

licensee's radiation protection program as required by 10 CFR Parts

Enclosure 2

0

26

20.1902. and 1904. The review included.observation of radiological

protection activities for control of radioactive material, including

pQstlngs and labeling, and radioactive waste processing.

b. Observations and Findings

At the time of the inspection. Unit 1 was shut down for a scheduled 54

day refueling outage (U1EOC17). The inspectors reviewed survey data of

radioactive material storage areas. Observations and survey results

determined the licensee was effectively controlling and storing

radioactive material and all material observed was appropriately labeled,

as required by 10 CFR Part 20.1904. The inspectors determined the

licensee was processing radioactive waste to maintain exposures As-Low

As-Reasonably-Achievable (ALARA) and to minimize quantities of

radioactive waste stored on site.

The inspectors also reviewed anddiscussed radioactive liquid processing

during tours of the radioactive waste (radwaste) facility and observed

part of a radioactive liquid discharge in progress. The licensee had

recently installed a new radwaste resin sluice system which allowed for

the transfer of spent resin from the Units 1, 2, and 3 spent fuel pools.

purification and deborating demineralizers to the resin batch tank

located in the Radwaste facility. The chief purpose of the modification

was to perform radwaste spent resin sluices inside of the facility and

not be affected by weather conditions. Another benefit of the

modification was that resin sluices could be performed in shorter times.

also minimizing personnel radiation exposure.

During tours of the auxiliary building and radioactive waste

storage/handling facilities, the inspectors observed the licensee had

performed radiological work in 2 onsite buildings, the reactor coolant

pump building and the ice blast building, not specified as monitored

pathways for radioactive material in the licensee's Offsite Dose

Calculation Manual.

The inspectors requested additional information

regarding the licensee's evaluations of the intended work scope to be

performed in the buildings and the associated radiological engineering

controls that would be applicable. Pending follow up information to be

provided and reviewed, one Unresolved Item (URI) was identified

concerning the applicability of monitoring requirements of Criterion 64

of 10 CFR 50 Appendix A and reporting requirements of 40 CFR 190 and 10

CFR 50.36a. This issue will be tracked by URI 50-269.270.287/97-15-03:

Determine the Applicability of Monitoring Requirements of Criterion 64

of 10 CFR 50 Appendix A and Reporting Requirements of 40 CFR 190 and 10

-*

CFR 50.36a.Regarding Potential of Unmonitored Release Pathways.

Enclosure 2

27

c. Conclusions

Based on observations and procedural reviews, the inspectors determined

the licensee was effectively maintaining controls for radioactive waste

and waste processing. One URI was identified to determine monito.ing

requirements for radiological work in two onsite buildings. The

licensee':s initiative to improve resin sluice processing systems to

maintain exposures ALARA and to improve environmental controls for resin

sluicing was viewed as a strength.

R1.2 Water Chemistry Controls

a. Inspection Scope (84750)

The inspectors reviewed implementation of selected elements of the

licensee's water chemistry control program for monitoring primary and

secondary water quality as described in the TS limits, the Station

Chemistry Manual, and the UFSAR. The review included examination of

program guidance and implementing procedures, as well as analytical

results for selected chemistry parameters.

b. Observations and Findings

The inspectors reviewed selected analytical results recorded for Units

1, 2 and 3 reactor coolant and secondary samples taken between August 1,

1997, and October 31, 1997. The selected parameters reviewed for

primary chemistry included dissolved oxygen, chloride, pH. and fluoride.

The selected parameters reviewed for secondary chemistry included

hydrazine, iron, and chloride. Those primary parameters reviewed were

maintained well within the relevant TS limits for power operations.

Those secondary parameters reviewed were maintained according to station

procedures. During tours, the inspectors also observed the licensee

performing primary system chromate sampling in accordance with licensee

procedures. The inspectors observed that the licensee exercised good

radiological work practices during the sampling evolution.

c. Conclusions

Based on the above reviews, it was concluded that the licensee's water

chemistry control program for monitoring primary and secondary water

quality had been effectively implemented, for those parameters reviewed,

in accordance with the TS requirements and the Station Chemistry Manual

for Pressurized Water Reactor water chemistry.

Enclosure 2

28

R1.3 Transportation of Radioactive Materials

a. Inspection Scope (86750, TI 2515/133)

The inspectors evaluated the licensee's transportation of radioacpive

materials programs for implementing the revised Department of

Transportation.(DOT) and NRC transportation regulations for shipment of

radioactive materials as required by 10 CFR 71.5 and 49 CFR Parts 100

through 177.

b. Observations and Findings

The inspectors reviewed and discussed licensee procedures and computer

tracking systems and determined that they adequately addressed the

following: assuring that the receiver has a license to receive the

material being shipped: assigning the form., quantity type, and proper

shipping name of the material to-be shipped: classifying waste destined

for burial: selecting the type of package required: assuring that the

radiation and contamination limits are met: and preparing shipping

papers.

Licensee's records for three shipments of radioactive material performed

since the last inspection of this area were reviewed and the inspectors

determined the shipping papers contained the required information. The

inspectors also determined the licensee had maintained records of

shipments of licensed material for a period of three years after

shipment as required by 10 CFR 71.91(a). In addition, the licensee

possessed a current certificate of approval (NRC Form 311) for their

"Quality Assurance Program Description for Radioactive Material Shipping

Packages Licensed Under 10 CFR 71."

c. Conclusions

Based on the above reviews, the inspectors determined that the licensee

had effectively implemented a program for shipping radioactive materials

required by NRC and DOT regulations.

R2

Status of RP&C Facilities and Equipment

R2.1 Meteorological Monitoring Proqram

a. Inspection Scope (84750)

-.

Section 2.3.3.2 of the UFSAR described the operational and surveillance

requirements for the meteorological monitoring instrumentation.

Enclosure 2

29

b. Observations and Findings

The inspectors toured the control room with cognizant.1 icensee personnel

and determined thatthe-meteorological instrumentation was operable and

that data for wind speed, wind direction, air temperature, and

,

precipitation were being collected as described in the UFSAR. -Records

revealed that the licensee had maintained-a high level of operability

for meteorology equipment during 1997. Wind speed and wind direction at

10 and 60 meters was operable approximately 99.3 percent, air

.

temperature approximately 99.3 percent, and precipitation 99.6 percent.

c. Conclusions

Based on the above reviews and observations, it was concluded that the

meteorological instrumentation had been adequately maintained and that

the meteorological monitoring program had been effectively implemented.

R7

Quality Assurance in Radiological Protection and Chemistry Activities

R7.1 Quality Assurance in Radiation Protection and Chemistry

a. Inspection Scope (84750, 86750)

10 CFR 20.1101 requires that the licensee periodically review the

radiation protection (RP) program content and implementation at least

annually. Licensee periodic reviews of the RP program were reviewed to

determine the adequacy of identification and corrective actions.

b. Observations and Findings

The inspectors reviewed the most recent QA audits in the area of RP.

chemistry, and transportation. These audits were accomplished by

reviewing RP procedures, observing work, reviewing industry

documentation, and performing plant walkdowns to include surveillance of

work areas by supervisors and technicians during normal work coverage.

The inspectors also reviewed documentation of potential radiological

problems or areas for improvement through the licensee's PIP.

c. Conclusions

The inspectors determined that the licensee was performing QA audits and

effectively assessing the radiation protection program as required by 10

CFR Part 20.1101. The inspectors also determined that the licensee was

- -

completing-corrective actions in a timely manner.

Enclosure 2

0II

30

R8

Miscellaneous Radiation Protection & Chemistry Issues (92904)

R8.1 (Closed) URI 50-269,270,287/97-01-07: Failure to Meet Requirements of

10 CFR 70.24

This issue involved the failure to have in place either a criticatity

monitoring system for storage and handling of new (non-irradiated) fuel

or an NRC approved exemption to this requirement contained in 10 CFR

70.24.

10 CFR 70.24 requires that each licensee authorized to possess more than

a small amount of special nuclear material (SNM) maintain in each area

in which such material is handled, used, or stored a criticality

monitoring system which will energize clearly audible alarm signals if

accidental criticality occurs. The purpose of 10 CFR 70.24 is to ensure

that, if a criticality were to occur during the handling of SNM,

personnel would be alerted to that fact and would take appropriate

action.

Most nuclear power plant licensees were granted exemptions from 10 CFR

70.24 during the construction of their plants as part of the Part 70

license issued to permit the receipt of the initial core. Generally,

these exemptions were not explicitly renewed when the Part 50 operating

license was issued, which contained the combined Part 50 and Part 70

authority. In August 1981, the Tennessee Valley Authority (TVA), in the

course of reviewing the operating licenses for its Browns Ferry

facilities, noted that the exemption to 10 CFR 70.24 that had been

granted during the construction phase had not been explicitly granted in

the operating license. By letters dated August 11. 1981, and August 31,

1987, TVA requested an exemption from 10 CFR 70.24. On May 11, 1988,

NRC informed TVA that "the previously issued exemptions are still in

effect even though the specific provisions of the Part 70 licenses were

not incorporated into the Part 50 license." Notwithstanding the

correspondence with TVA, the NRC has determined that, in cases where a

licensee received the exemption as part of the Part 70 license issued

during the construction phase, both the Part 70 and Part 50 licenses

should be examined to determine the status of the exemption. The NRC

view now is that unless a licensee's licensing basis specifies

otherwise, an exemption expires with the expiration of the Part 70

license. The NRC intends to amend 10 CFR 70.24 to provide for

administrative controls in lieu of criticality monitors.

The NRC has concluded that a violation of 10 CFR 70.24 existed. The NRC

--

has also determined that numerous other licensees have similar

circumstances that were caused by confusion regarding the continuation

of an exemption to 10 CFR 70.24 originally issued prior to issuance of

'the Part 50 license. After considering all the factors that resulted in

'-these violations, the NRC has concluded that while a violation did

Enclosure 2

31

exist, it is appropriate to exercise enforcement discretion for

Violations Involving Special Circumstances in accordance with

Section VII B.6 of the "General Statement of Policy and Procedures for

NRC Enforcement Actions"-(Enforcement Policy), NUREG-1600.

Fl

Conduct of Fire Protection Activities

F1.1 Licensee Identified Fire Protection Discrepancies

a. Inspection Scope (64704)

The inspectors reviewed the adequacy of the licensee's evaluations and

corrective actions on the following licensee identified fire protection

discrepancies in which PIP reports had been issued.

PIP No.

PIP Description

3-097-1483

Failure to Install Fire Detection in New Unit 3

Computer Room

0-097-1484

High Pressure Service Water (HPSW)/Fire Pump Enclosure

Was Not 3-Hour Fire Rated Construction

5-097-2667

Inoperable Fire Door Between Turbine and Auxiliary

Buildings

0-097-2806

Fire Protection Valves for Hose Stations Were Not

Stroke Tested

1-097-3309

Obstructed Fire Detectors in Unit 1 Reactor Building

b. Observations and Findings

The licensee's evaluations on these PIP discrepancies were thorough and

corrective action was appropriate. These identified discrepancies

demonstrated that the licensee's fire protection staff was performing

detail assessments of the site's fire protection program and were taking

appropriate action to identify the cause and take corrective action on

identified discrepancies. The inspector's observations and findings on

each of these PIP items are as follows:

PIP 3-097-1483: This issue involved the failure to extend the

automatic fire detection system to provide coverage for a new

computer room in the Unit 3 control room complex. The corrective

action for this PIP included the installation of automatic fire

detection for the Unit 3 computer room addition. In addition, the

modification in process for the Unit 1 and 2 computer rooms was

revised to include the installation of automatic fire detectors.

Enclosure 2

32

Section 9.5.1.5 of the Oconee UFSAR states that fire detector

locations were selected based on engineering judgement to monitor

areas containing vital equipment. The computer rooms adjacent to

the control rooms were not initially provided with automatic fire

detection coverage. but. the fire detection system. was provided for

this area during the upgrades to the plant fire alarm system in

the early 1990s.

Since the computers were not considered vital

equipment, automatic fire detection was not required to be

provided for this area during the NRC licensing review. This is

documented by the NRC Fire Protection Safety Evaluation Report

dated August 11, 1978. The cause for not providing fire detector

coverage for this area was identified by the licensee as a design

oversight since this area was not initially provided with fire .

detector coverage. Therefore, although.providing fire detector.

coverage for the computer rooms adjacent to the control room

complex is a good fire protection practice, the failure to

provided fire detection for these areas is outside the NRC

licensing basis for Oconee.

The inspector considered the licensee's identification and

correction of this problem as proactive.

PIP 0-097-1484: During a routine surveillance, the licensee

identified that the concrete roof construction of the HPSW/fire

pump room enclosure was equivalent to 1-hour fire rated

construction whereas the walls for these rooms had a 3-hour fire

rating.

Section 9.5.1.5.2 of the Oconee UFSAR states, "The HPSW pumps are

located in separate concrete block structures with power cables to

the motors being embedded in concrete floor. Separation is by

fire rated wall assemblies." The Oconee Fire Protection Safety

Evaluation Report dated August 11, 1978, states, "The HPSW pumps

are located in the turbine building, each in a small masonry room

enclosing the pump and motor... We find the basic water supply

system satisfies the provision of Appendix A to Branch Technical

Position (BTP) 9.5-1 and is,

therefore, acceptable."

The inspector reviewed the Oconee fire barrier drawing series

0-310K and 0-310L and noted that the drawings indicated a 3-hour

fire wall enclosure for the pumps. but did not address the fire

rating of the roofs/ceilings for the pump enclosures. The

licensee's PIP evaluation found the "as built" configuration

satisfactory since: (1)

HPSW pump rooms would not be exposed to

turbulent flame impingement from an oil pool fire; (2)

automatic

sprinkler systems installed in Turbine Building would cool, dilute

and suppress an oil pool fire before the fire reached the pump

Enclosure 2

33

rooms; (3)

combustible materials were not located on the under

side of the pump.room ceilings;-and (4)

heat from oil pool fire

which wasrnot'completely suppressed by the fire suppression system

would dissipate to the open Turbine Building and .would not

concentrate at the roofs of the HPSW .pump rooms.

Them Jnspector performed 'a walkdown inspection of the Turbine

Building and concluded that the licensee's evaluation and the fire

protection features provided for the areas were appropriate for

the hazards involved and should assure that a fire within the

Turbine Building would not damage both HPSW pumps.

The licensee issued PIP 0-097-3920 to add a note on the applicable

drawings for.drawing series 0-310K and 0-31OL-to indicate the fire

rating of the ceilings/roofs of the HPSW pump rooms had a 1-hour

fire resistance rating.

The fire resistance rating of the HPSW pump rooms was not an NRC

licensing issue: therefore, this item is not a regulatory issue.

The licensee's identification and evaluation for resolution were

considered positive actions.

PIP 5-097-2667: This issue was related to inoperable fire door

No. 325 on the 796' elevation of the Auxiliary Building. On

August 25, 1997. a member of the licensee's staff found door

number 325 with the locking mechanism removed, grey tape was

placed over the missing locking mechanism, and a plastic tie wrap

was being used for a handle. Operations personnel acknowledged

that this door had been in this configuration for at least one

day, and possibly longer, and that a work order had not been

issued to repair the door. Also, the door had not been declared

inoperable and the compensatory actions of UFSAR Section 16,

Selected Licensee Commitments (SLC). Item 16.9.5. Fire Barriers,

had not been implemented.

Paragraph 3.E of the Oconee Operating License states that the

licensee shall implement and maintain in effect all provisions of

the approved fire protection program as described in the UFSAR and

as approved in the SERs (i.e., NRC's Fire Protection Safety

Evaluation Reports).

For inoperable fire barriers, UFSAR SLC 16.9.5 Action Item a.ii

required verification that the area fire detection system was

operable and the establishment of an hourly fire watch patrol for

the area. Door 325 was located in a high traffic area; therefore,

there were many opportunities during the work day for any of the

many site employees who passed through this door to recognize that

Enclosure 2

34

the door was inoperable and to submit a work order to perform the

required repairs.

The.failure to promptly identify this inoperable fire barrier

penetration and to implement the appropriate compensatory measures

of UFSAR SLC 16.9.5 is a violation. However, this non-repetitive,

licensee identified and corrected violation is being treated as a

Non-Cited Violation (NCV). consistent with Section VII.B.1,of the

NRC Enforcement:Policy and is identified as NCV 50-269,270.287/97

15-04:

Inoperable Fire Door With No Compensatory Measures.

PIP 0-097-2806: During a review of Procedure MP/0/A/1705/032.

Fire Hose Stations., which was performed in September 1997, the

licensee's reviewer noted that the hose station valves had not

been stroke tested as required by the procedure.

The licensee reviewed the completed procedures for MP/0/A/1705/032

from 1992. through 1996 and noted that none of these procedures had

stroke tested or cycle tested the valves associated with the fire

hose system. All of the hose stations listed by UFSAR SLC 16.9.4

and SLC Table 16.9.4 were flushed and stroke tested on September

12, 1997. This demonstrated that adequate flow was available and

the valves and hose stations were operable. All additional fire

hose stations installed in facility were satisfactorily flushed

and valves were stroke tested on October 24, 1997. Enhancements

were made to the procedure to prevent recurrence. The licensee

attributed the cause of this event as a human performance error.

Personnel assigned the task of performing surveillance tests and

inspections on the fire hose system were provided with additional

training on the expectations and acceptance criteria for the fire

hose system.

Paragraph 3.E of the Oconee Operating License states. "The

licensee shall implement and maintain in effect all provisions of

the approved fire protection program as described in the UFSAR and

as approved in the SERs" (i.e., NRC's Fire Protection Safety

Evaluation Reports).

UFSAR SLC Section 16.9.4, Surveillance Item a.iii, states, "At

least tri-annually, the fire hose station valves shall be partial

stroke tested."

The failure to stroke test the valves for the fire hose station

- -

system in accordance with UFSAR SLC 16.9.4 is a violation.

However, this non-repetitive, licensee identified and corrected

violation is being treated as a Non-Cited Violation, consistent

with Section VII.B.1 of the NRC Enforcement Policy and is

Enclosure 2

35

identified as NCV-50-269,270.287/97-15-05:

Failure to Stroke Test

the Fire Hose Station Valves.

PIP r-097-3309. This issue was related to covering the smoke

detector devices in the Unit 1 RB with a plastic material to

prevent damage to the detectors during the wash down of the RB

while the unit was in a refueling outage. Most of the detectors

were only partially covered with the plastic material.

These

smoke detectors would have been able to perform their intended

function. However, on September 18. 1997, two adjacent detectors

located on the west side of the second floor of the Unit 1 RB were

completely enclosed with the plastic material and would not have

performed their intended function. On October 2. 1997, during the

performance of fire detection surveillance testing, the testing

personnel found these obstructed detectors were not capable of

performing their intended function and the RB fire detection

system was declared inoperable. The plastic material was removed

from these detectors and the system was restored to an operable

condition. The licensee determined the cause of this event to be

poor program design and work process implementation. The

requirement for maintaining the operability of the Reactor

Building fire detection systems and the required implementation of

compensatory actions for inoperable fire detection systems were

discussed with the appropriate personnel.

The inoperable smoke detectors were located in an area which

contained electrical cables to components needed to assure

reliable decay heat removal and were required to be operable.

Paragraph 3.E of the Oconee Operating License states. "The

licensee shall implement and maintain in effect all provisions of

the approved fire protection program as described in the UFSAR and

as approved in the SERs" (i.e.. NRC's Fire Protection Safety

Evaluation Reports).

UFSAR SLC Section 16.9.6, Fire Detection Instrumentation, Action

Item a states. "When more than 50% of the provided detectors for

each equipment/location, or any 2 adjacent detectors for each

equipment/location as shown in Table 16.9-6 are not OPERABLE.

appropriate action shall be taken consisting of:

within 1-hour, a

fire watch patrol shall be established to inspect the accessible

equipment/location at least once per hour or as permitted by Site

Directives." Table 16.9-6 lists the detectors provided for the RB

.

as required to be operable.

u 2

Enclosure 2

0

36

The failure to implement the, compensatory action requirements for the

inoperable fire detection system in the Unit 1 RB in accordance with

UFSAR .SLC 16.9.6 is a violation. However, this non-repetitive, licensee

identified and corrected violation is being treated as a Non-Cited

Violation, consistent with Section VII.B.1 of the NRC Enforcement Policy

and is identified as NCV 50-269/97-15-06: Failure to Implement the

Compensatory Action Requirements for the Inoperable Fire Detection

System in the Unit 1 Reactor Building.

c. Conclusions

The licensee's fire protection staff demonstrated an aggressive attitude

in the identification and correction of fire protection deficiencies.

However, three Non-Cited Violations were identified for the licensee's

failure to meet the fire protection operability requirements for three

required fire protection features.

F2

Status of Fire Protection Facilities and Equipment

F2.1 Operability of Fire Protection Facilities and Equipment

a. Inspection Scope (64704)

The inspectors reviewed the impairment log for fire protection

components and features to assess the licensee's performance for

returning degraded fire protection components to service. In addition,

walkdown inspections were made to assess the material condition of the

plant's fire protection systems, equipment, features and fire brigade

equipment.

b. Observations and Findings

Operability of Fire Protection Equipment and Components

As of November 6, 1997, there were only five fire protection components

listed on the impairment log as degraded. The following items were

identified as inoperable: one smoke detector located in the Unit 1 RB,

two smoke detectors in the Unit 2 RB. one smoke detector in the Unit 3

RB and the fire hose stations in the Unit 1 RB.

The fire detection systems for the RB were considered operable by UFSAR

SLC Section 16.9.6 since more than 50 percent of the detectors were

operable and no two adjacent smoke detectors were inoperable. The

inoperable smoke detectors were scheduled to be replaced during the next

available outage.

Enclosure 2

37

For the inoperable Unit 1 RB hose stations, the licensee was maintaining

a minimum of four fire extinguishers adjacent to the personnel hatch

entrance to the RB from the Auxiliary Building. This met the

requirements of UFSAR .SLC Section 16.9.4 Action Item b.

-The.,hose

stations for the Unit 1 RB were inoperable due to modifications i9

process on the low pressure service during the current refueling outage.

The inspectors reviewed previous impairments listed in the fire

protection impairment log and noted that a .high priority had.been placed

on restoring inoperable fire protection features to service. Most of

the inoperable features had been restored to service within 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br />.

The inspectors toured the plant and noted that the material condition of

the: fire protection systems'was good and that the systemswere well

maintained.

Fire Brigade Equipment

The turnout gear for the fire brigade members was stored in lockers

adjacent to the two control rooms.

Each fire brigade member was

assigned his own personal turnout gear, consisting of a coat, pants,

boots, gloves, etc. A sufficient number of turnout helmets were

provided to equip the fire brigade members expected to respond in the

event of a fire or other emergency. This equipment was properly stored

and was well maintained.

Additional fire fighting equipment was stored on a motorized fire and

rescue vehicle and an equipment trailer stored outside the protected

area adjacent to the main administration buildings. An equipment

storage trailer and another trailer equipped with foam fire fighting

equipment were stored inside the protected area, north of the Radwaste

Building. Fire fighting equipment was also stored on carts located on

the generator level of the Turbine Building adjacent to Unit 1 and 2

control rooms and Unit 3 control room. Fire hose, nozzles, and

miscellaneous fire fighting equipment was stored on the vehicle,

trailers and equipment carts. This equipment was properly stored and

was well maintained.

c. Conclusions

The low number of inoperable or degraded fire protection components, in

conjunction with the good material condition of the fire protection

components and fire brigade equipment, indicated that appropriate

emphasis had been placed on the maintenance and operability of the fire

protection equipment and components.

Enclosure 2

38

F2.2 Surveillance of Fire Protection Features and Equipment

a. Inspection Scope (64704)

The inspectors reviewed the following completed surveillance and rest

procedures:

PT/0/A/0250/24. Fire Protection System Three Year Flow Test,

Revisions 12 to 15: performed October 14, 1996,and April 3 and 18.

1997..

PT/0/A/0250/25, High Pressure Service Water and Fire Protection

Flow Test, Revision 18; performed May 30. 1997.

PT/0/A/0250/35, Radwaste Contaminated Oil Tank Skid Areas

Sprinkler System Test, Revision 5: performed August 26, 1997.

PT/1/A/2200/006, Keowee Hydro Unit 1 C02 Fire Protection System

Three Year Flow Test. Revision 8: performed January 15, 1997.

PT/1/A/2200/006, Keowee Hydro Unit 2 C02 Fire Protection System

Three Year Flow Test, Revision 8: performed June 13, 1996 and July

30, 1996.

PT/0/A/2200/014, Keowee C02 System Test, Revision 11: performed

May 23, 1997.

TT/0/A/06201/031, Keowee Fire Pump Performance Verification Test

for CIGNA and Flow Meter Verification, Revision 0: performed June

4. 1997.

b. Observations and Findings

The completed fire protection surveillance tests reviewed by the

inspectors had been appropriately completed and met the acceptance

criteria. The test procedures were adequate to perform the fire

protection surveillance requirements specified by UFSAR Chapter 16.9,

SLC.

c. Conclusions

Adequate surveillance and test procedures were provided for the fire

protection systems and features, and implementation of the procedures

was effective.

Enclosure 2

39

F2.3 Fire Barrier Penetration Seals

a. Inspection Scope (64704)

The inspectors reviewed the installation of the following fire barrier

penetration seals to determine if the installed penetration seals met

the design documents and were bounded by configurations which

satisfactorily passed a fire-test which met the requirements of N C

Generic Letter 86-10 and NRC Information Notices, 88-04, 88-56 and. 94

28:

PENETRATION NO.

LOCATION

TYPE

SIZE (Inches)

1-M-S-2-A1

Cable Room

Silicone Foam

40x36

1 MS-8-Al

Cable Room

Silicone Foam

22x68

1-M-S-10-A1

Cable Room

Silicone Foam

1

1-M-F-17-A1

Cable Room

.. Silicone Foam

18x18

1-N-F-2-A1

Equipment Room

Silicone Foam

26x28

1-N-F-19-A1

Cable Shaft

Silicone Foam

60x96

1-P-E-2-A1

Penetration Room Silicone Foam

48x48

2-M-F-33-A1

Cable Room

Monocoat

14

2-M-N-3-A1

Cable Room

Silicone Foam

36x48

2-M-W-2-A1

Cable Room

Grout

1

3-P-E-4-A1

Penetration Room -Silicone Foam

41x42

b. Observations and Findings

The inspectors inspected each of the above penetrations and reviewed the

licensee's design, construction and surveillance inspection records for

these penetration seals. The silicone type penetration seals were

covered by 1-inch thick ceraform damming boards: therefore, it was

difficult to verify the specific design specifications that had been

used during the installation of these penetration seals.

The design and

construction documents permitted several installation seal options to

meet the design requirements. The specific requirements were dependent

on the barrier construction, thickness of the barrier, and whether the

penetratioi was through a wall or floor fire barrier.

The licensee had begun a project to revalidate the installation of these

penetration seals to determine if each penetration was bounded by a

Enclosure 2

40

specific design specification that was substantiated by qualified test

documents. During this inspection the licensee initiated PIP 0 097

3922 to expedite the completion of this project. The fire barrier

penetration seals for each unit were scheduled to be revaluated

following completion of their next scheduled refueling outage (i.g.,

early 1998 for Unit 1. Summer 1998 for Unit 2. and Winter 1999 for

Unit 3).

The licensee considered the fire barrier penetration seals to-be

operable based on the previous inspections performed following each

refueling outage using Procedure MP/1,2,3/A/1750/018. Fire Protection

Penetration Fire Barrier Inspection, (current Revisions 27, 20, 21 for

Units 1. 2. and 3, respectively). These procedures required an

inspection of each fire-barrier penetration following a unit's refueling

outage. In addition, in 1984 the licensee identified a number of

discrepancies associated with the facility's fire barrier penetration

seals, such as seals improperly installed, cracked, or missing (i.e..

actually not installed). Major modification work was required to

restore the penetration seals to operable status. Following these

modification activities, documentation was apparently not provided to

indicate the-design specification used for each penetration seal

installation.

This issue will be evaluated during a subsequent NRC inspection, upon

completion of the licensee's revalidation of the installation of the

fire barrier penetration seals. This is identified as Inspector

Followup Item (IFI) 50-269.270,287/97-15-07: Review of Licensee's

Revalidation of Fire Barrier Penetration Seals.

c. Conclusion

The inspector concluded that the fire barrier penetration seals were

functional.

However, the licensee had implemented a project to provide

sufficient documentation to indicate the seal installations met the

design specifications and were bounded by tested configurations.

F3

Fire Protection Procedures and Documentation

F3.1 Fire Fighting Fire Pre-Plans

a. Inspection Scope (64704)

The inspectors reviewed the following procedures for compliance with the

NRC requirements and guidelines:

Nuclear Station Directive (NSD) 112, Fire Brigade Organization.

Training and Responsibilities. Revision 0

Enclosure 2

41

NSD 313, Control of Combustible and Flammable Materials,

Revision 0

NSD 314, Hot Work Authorization, Revision 0

Oconee Site Directive 3.2.9, Reporting of Fire Protection.

Impairments, Revision 1/30/96

Pre-Fire Plans, Oconee Pre-Fire Plans and Procedures

Plant tours were also performed to assess procedure compliance.

b. Observations and Findings

The above procedures were the principal procedures issued to implement

the facility's fire protection program. These procedures contained the

requirements for program administration, controls over combustibles and

ignition sources, fire brigade organization and training, and

operability requirements for the fire protection systems and features.

The procedures were well written and met the licensee's commitments to

the NRC. except for the Pre-Fire Plans. Pre-Fire Plans had not been

provided for all plant areas containing safety-related components.

The inspectors performed plant tours and noted that even though the

plant was in a refueling outage, implementation of the site's fire

prevention program for the control of ignition sources, transient

combustibles were good with overall general housekeeping considered

satisfactory. Appropriate fire prevention controls were being applied

to the accumulation of transient combustible materials, the number of

maintenance activities and welding operations in process due to the

refueling outage.

During this inspection, the inspector noted that there were a number of

areas within the plant which contained or presented a hazard to safety

related components in which the licensee had not developed fire fighting

procedures. For example, fire fighting procedures had not been provided

for the Unit 3 low pressure injection hatch area on the 771-foot

elevation of the Auxiliary Building. This area contained electrical

components for the low pressure injection and component cooling systems

and presented an exposure fire hazard to the Unit 3 low pressure and

high pressure injection pumps.

Paragraph 3.E of the Oconee Operating License states that the licensee

-

-shall

implement and maintain in effect all provisions of the approved

fire protection program as described in the UFSAR and as approved in the

SERs (i.e.. NRC's Fire Protection Safety Evaluation Reports).

Enclosure 2

42

The licensee's January 6, 1978, fire protection submittal to the NRC

stated that -"in lieu of fire fighting procedures," general arrangement

drawings of-all levels within the station and yard areas have been

marked showing the location-of fire protection equipment and the

location of combustibles. These drawings have been located in each

control.room and in the Safety Supervisor's office. We intend to expand

the information on these drawings to indicate additional combustibles,

hazards and ventilation systems supplying each location."

NRC's August

11, 1978.Fire Protection Safety Evaluation Report, Section C.6.6 found

the licensee's proposed actions to provide "the necessary strategies for

fighting fires in~safety-related areas and areas presenting a hazard to

safety related equipment" to be acceptable.

However, the licensee had not provided the necessary strategies for

fighting fires in all safety-related areas and areas presenting a hazard

to safety-related equipment. This is identified as VIO 50

269,270,287/97-15-08:

Fire Fighting Strategies Not Provided for All

Safety-Related Areas.

The licensee had previously identified this problem and had developed

fire fighting procedures for all safety-related and important plant

areas. These procedures had not been issued due to several needed

enhancements. PIP 0-097-3921 was issued during this inspection to

address this issue and to expedite completing the revisions to these

procedures. Revisions to these procedures were scheduled to be

completed by June 1998.

c. Conclusions

In general, the fire protection program implementing procedures were

well written and met the licensee's commitments to the NRC requirements.

Procedure implementation for the control of ignition sources and

transient combustibles was good. Overall, general housekeeping was

satisfactory. However, a violation was identified involving the failure

to provide fire fighting strategies for all plant areas which contained

safety-related equipment or presented an exposure hazard to safety

related components.

F5

Fire Protection Staff Training and Qualification

F5.1 Fire Brigade

a. Inspection Scope (64704)

The inspectors reviewed the fire brigade organization and training

program for compliance with the NRC guidelines and requirements.

Enclosure 2

43

b. Observations and Findings

The organization and training requirements for the plant fire brigade

Were established by NSD 112. Fire Brigade Organization, Training and

Responsibilities, Revision 0. The fire brigade for each shift was,

composed of a fire brigade leader and at least four brigade members from

operations and approximately five members from maintenance. The fire

brigade leader was a senio' reactor operator (SRO)

and was normally one

of the unit shift supervisors. The other members from operations were

non-licensed plant operators. One of the fire brigade members was

normally assigned the duties of fire brigade safety officer to provide

technical and administrative assistance to the fire brigade leader and

to help assure the safe performance of each fire brigade member by

checking each member for appropriate dress out prior to entering the

fire area, maintaining records of each fire brigade exposure to fire or

radiation hazards, use of self-contained breathing apparatus, and

reviewing the pre-fire plans during the emergency for assurances that

appropriate measures are being followed for compliance with applicable

safety and fire hazards in the area. Assignment of a fire brigade

safety officer was identified as a program strength.

Each fire brigade member was required to receive initial, quarterly and

annual fire fighting related training and to satisfactorily complete an

annual medical evaluation and certification for participation in fire

brigade fire fighting activities. In addition, each member was required

to participate in at least two drills per year. The initial and annual

fire fighting training was provided by the fire science department of a

local college.

As of the date of this inspection, there was a total of 26 operations

trained fire brigade leaders and 73 operations personnel and 32

maintenance personnel on the plant's fire brigade. Approximately five

fire brigade leaders, eight operations fire brigade members and five

maintenance fire brigade members were assigned to each of the five

operations crews. This was a sufficient number to meet the staffing

requirements for the plant operations and the facility's fire brigade

complement of one team leader and nine members per shift.

The inspectors reviewed the training and medical records for the fire

brigade members and verified that the training and medical records were

up to date. The facility utilized off-site qualified state certified

fire brigade training instructors and a state fire training facility to

perform the annual fire brigade training and practical fire training

scenarios.

During this inspection, the inspectors witnessed a fire brigade drill on

November 4, 1997, involving a simulated fire in an electrical panel

'

located in Room 159. low pressure hatch area on the 771 foot elevation

Enclosure 2

44

of the auxiliary building.

The response of the fire brigade to the

simulated fire was mixed. Shortcomings were identified in the

performance of the fire brigade members and the safety officer. After

these shortcomings were resolved, the subsequent drill performance was

satisfactory. These shortcomings were identified by the licensee,

discussed in the post-drill critique, and documented in PIP 0-097-3950

for resolution.

Based upon a review of the licensee's May 1995 QA Triennial Fire

Protection Audit, a review of ten previous-fire brigade drill summaries,

and an NRC resident inspector witnessed drill documented in NRC IR 50

269.270,287/97-12 these shortcomings were not typical or a trend.

c.

Conclusions.

The fire brigade organization and training met the requirements of the

site procedures. The use of the fire brigade safety officer position

during fire emergencies was identified as a program strength. Licensee

performance during a fire brigade drill conducted during the period was

mixed.

F7

Performance in Fire Protection Activities

F7.1 Review of Triennial Fire Protection Audit

a. Inspection Scope (64704)

The inspector reviewed Triennial Fire Protection Audit, SA-95

24(ON)(RA), which was conducted May 15 through June 8. 1995.

b. Observations and Findings

Audit SA-95-24(ON)(RA) was a triennial QA audit of the facility's fire

protection program. The licensee informed the inspector that this was

the most recent comprehensive audit of the fire protection program.

Duke's December 18. 1991, letter to the NRC stated that performance

based criteria were to be used for establishing audit frequencies at the

Duke facilities. NRC's letter dated May 7. 1992, documented that this

was satisfactory. Previously, the TS had required annual, biannual and

triennial audits of the fire protection program. However, based on the

licensee's assessment of good fire protection performance, the most

recent audit performed of the Oconee fire protection program was the

1995 triennial audit. As documented in NRC Inspection Report 50

413,414/97-07 for Catawba, the NRC is re-evaluating this issue.

The inspectors reviewed the audit findings from the 1995 QA report and

the corrective actions taken on the identified discrepancies. The

report indicated that a comprehensive audit had been performed and seven

Enclosure 2

45

findings were identified. The inspector reviewed the status of each of

these items and verified that the.corrective action on each finding had

been completed.

c. Conclusions

The,1995 audit and assessment of the facility's fire protection program

were comprehensive and appropriate corrective action was promptly, taken

to resolve identified issues.

V. Management Meeting s

Xl

Exit Meeting Summary

The inspectors presented the inspection r-sulis to members of licensee

management at the conclusion of the inspection on November 18. 1997.

The licensee acknowledged the findings presented. Dissenting comments

were received from the licensee and resolved by the NRC. Proprietary

information is not contained in this report.

Partial List of Persons Contacted

Licensee

D.

Brandes, Consultant Engineer, Nuclear Engineering

E. Burchfield, Regulatory Compliance Manager

T. Coutu, Scheduling Manager

D. Coyle. Mechanical Systems Engineering Manager

T. Curtis, Operations Superintendent

B. Dobson, Mechanical/Civil Engineering Manager

W. Foster, Safety Assurance Manager

D. Hubbard, Maintenance Superintendent

C. Little. Electrical Systems/Equipment Engineering Manager

W. McCollum, Vice President, Oconee Site

M. Nazar. Manager of Engineering

B. Peele, Station Manager

J. Smith, Regulatory Compliance

NRC

D. LaBarge, Project Manager

Inspection Procedures Used

IP37550

Engineering

IP37551

Onsite Engineering

IP37828

Installation and Testing of Modifications

Enclosure 2

46

W

IP40500

Effectiveness of Licensee Controls In Identifying and Preventing

Problems.

TI-P50002

Steam Generators

IP61726

Surveillance Observations

IP62700

Maintenance Program Implementation

IR62707

Maintenance Observations

4(P64704

Fire Protection Program

IP71707

Plant Operations

IP71714

Cold Weather Preparations

IP71750

Plant Support Activities

fP8f750e

Raoctive

aste 'T en

n

l

nt and Environmental

Monitr

Gi erat

MP84760

Solid Radioactive Waste Management and Transportation of

Radioactive Material

IP92903

Followup - Engineering

laSFol

u - Plant Support

Enclosure 2

47

Items Opened, Closed, and Discussed

50-269,287/97-15-01

VIO

Failure to Complete Required Technical

Specification Surveillances on LPI Flow

Instruments (Section M1.5)

50-269,270.287/97-15-02

URI

Valve Parts Identification Problem

(Section M2.1)

50-269,270V287/97-15-03,

URI: Determine the:Applicability of Monitoring

Requirements of Criterion 64 of 10 CFR 50

Appendix A and Reporting Requirements of

40 CFR 190 and 10 CFR 50.36a Regarding

Potential .of Unmonitored Release Pathways

(Section R1.1)

50-269,270,287/97-15-04

NCV

Inoperable Fire Door With No Compensatory

Measures (Section F1.1)

50-269,270,287/97-15-05

NCV

Failure to Stroke Test the Fire Hose

Station Valves (Section F1.1)

50-269/97-15-06

NCV

Failure to Implement the Compensatory

Action Requirements for the Inoperable

Fire Detection System in the Unit 1

Reactor Building (Section F1.1)

50-269,270,287/97-15-07

IFI

Review of Licensee's Revalidation of Fire

Barrier Penetration Seals (Section F2.3)

50-269,270,287/97-15-08

VIO

Fire Fighting Strategies Not Provided for

All Safety-Related Areas (Section F3.1)

50-270,287/97-15-09

VIO

Failure to Update the UFSAR Regarding Fuel

Enrichment (Section E8.3)

Closed

50-269,270,287/96-09-03

IFI

Expected End-of-Cycle Heat Loads (Section

E8.1)

-

50-269/97-03. Revs. 0 and 1 LER

Post LOCA Boron Dilution Design Basis Not

Met Due To Deficient Design Analysis

(Section E8.2)

Enclosure 2

0

48

50-269.270,287/97-01-07

URI

Failure to Meet Requirements of 10 CFR

70.24 (Section R8.1)

50-269.270,287/97-12-02

URI

Fuel Load UFSAR Statements (Section E8.3)

50-269.270,287/97-01-06

URI

Boron Dilution Flow Path Inoperability

(Section E8.2)

Discussed

50-269.270,287/96-13-03

IFI

Service Water Modifications (Section E3.1)

List of Acronymns

ABB

Asea Brown Boveri

ALARA

As Low As Reasonably Achievable

ANSI

American National Standard

ASME

American Society of Mechanical Engineers

BTP

Branch Technical Position

BWOG

Babcock and Wilcox Owners Group

BWST

Borated Water Storage Tank

CENO

Combustion Engineering Nuclear Operations

CFR

Code of Federal Regulations

CCW

Condenser Circulating Water

DC

Direct Current

DEI

Dominion Engineering, Incorporated

DOT

Department of Transportation

ECT

Eddy Current Testing

EPSL

Emergency Power Safeguards Logic

EWST

Elevated Water Storage Tank

FIP

Failure Investigation Process

FIT

Framatome Technologies. Inc.

GPM

Gallons Per Minute

HPSW

High Pressure Service Water

ICCM

Inadequate Core Cooling Monitor

IFI

Inspector Follow-up Item

IGA

Intergranular Attack

IR

Inspection Report

KV

kilovolt

LER

Licensee Event Report

LOCA

Loss of Coolant Accident

LPI

Low Pressure Injection

LPSW

-Low Pressure Service Water

MFB

Main Feeder Busses

MCE

Mechanical Civil Equipment Group

BMP

Maintenance Procedure

CdNorth Carolina

Enclosure 2

49

NCV

Non-Cited Violation

NDE

Non-Destructive Examination

NRC

Nuclear Regulatory Commission

NSD

Nuclear System Directive

OAC

Operator Aid Computer

OTSG

Once-Through-Steam-Generator

PDR

Public Document Room

PIP

Problem Investigation Process

PT

Performance Test

PWR

Pressurized Water Reactor

QA

Quality Assurance

QC

Quality Control

RB.

Reactor Building

RCP

Reactor Coolant Pump

RCS

Reactor Coolant System

REV

Revision

RP

Radiation Protection

SALP

Systematic Assessment of Licensee Performance

SER

Safety Evaluation Report

SFP

Spent Fuel Pool

SG

Steam Generator

SLC

Selected Licensee Commitment

SNM

Special Nuclear Material

SRO

Senior Reactor Operator

SSF

Safe Shutdown Facility

TDEFWP

Turbine Driven Emergency Feedwater Pump

TM

Temporary Modification

TS

Technical Specification

TT

Temporary Test

TVA

Tennessee Valley Authority

UFSAR

Updated Final Safety Analysis Report

URI

Unresolved Item

UTS

Upper Tube Sheet

V

Volt

VA

Virginia

VIO

Violation

WO

Work Order

Enclosure 2