ML15118A159

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Insp Repts 50-269/96-16,50-270/96-16 & 50-287/96-16 on 961006-1116.Violations Noted.Major Areas Inspected:Maint, Engineering & Plant Support
ML15118A159
Person / Time
Site: Oconee  Duke Energy icon.png
Issue date: 12/04/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML15118A156 List:
References
50-269-96-16, 50-270-96-16, 50-287-96-16, NUDOCS 9612170442
Download: ML15118A159 (37)


See also: IR 05000269/1996016

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos:

50-269. 50-270, 50-287. 72-04

License Nos:

DPR-38, DPR-47, DPR-55. SNM-2503

Report No:

50-269/96-16. 50-270/96-16. 50-287/96-16

Licensee:

Duke Power Company

Facility:

Oconee Nuclear Station, Units 1, 2 & 3

Location:

7812B Rochester Highway

Seneca, SC 29672

Dates:

October 6, 1996 - November 16, 1996

Inspectors:

M. Scott, Senior Resident Inspector

G. Humphrey, Resident Inspector

N. Salgado, Resident Inspector

N. Economos. Reactor Inspector

R. Freudenberger, Senior Resident Inspector

D. Forbes. Reactor Inspector

R. Carroll, Project Engineer

R. Baldwin, Reactor Inspector

P. Kellogg, Reactor Inspector

Approved by:

L. D. Wert, Acting Chief, Projects Branch 1

Division of Reactor Projects

Enclosure 2

9612170442 961204

PDR

ADOCK 05000269

G

PDR

EXECUTIVE SUMMARY

Oconee Nuclear Station, Units 1, 2 & 3

NRC Inspection Report 50-269/96-16,

50-270/96-16, 50-287/96-16

This integrated inspection included aspects of licensee operations,

engineering, maintenance, and plant support. The report covers a six-week

period of resident inspection: in addition, it includes the results of

announced inspections by two regional safety inspectors, one visiting senior

resident, and one project engineer.

Operations

The Unit 1 shutdown and associated rod drop test was performed in

a professional and controlled manner. (Section 01.2)

Unit 2 midloop operation was well controlled and coordinated.

(Section 01.3)

The overall cold weather protection program was determined to be

adequate. (Section 01.4)

A Non-Licensed Operator was aggressive in the identification of a

discrepant condition on safety-related equipment. (Section 04.1)

0

Initial review of operator training associated with Integrated

Control System modifications indicated that the training was

adequate. An inspector followup item was identified to address

licensed operator qualification issues associated with the

modification.

Maintenance

Specific observed maintenance activities were generally performed

thoroughly and professionally. (Sections M1.1 and M1.2)

The licensee's welding instruction and field inspection programs

were appropriate. The licensee's efforts to identify and document

field conditions following the Unit 2 water hammer event were

commensurate with applicable code requirements and quality

standards, and reflected a conservative attitude. (Section M1.3)

Inservice Inspection examinations scheduled for this outage were

being performed as required by well trained personnel following

procedures written in compliance with applicable code

requirements. Personnel performing the inspections were well

qualified to execute their assigned tasks. Eddy current

examinations were consistent with Technical Specifications (TS)

4.17 requirements. Three tubes were identified in Steam Generator

"B"

with primary water stress corrosion cracking indications in

the roll transition region of the upper tubesheet. A decision had

not been reached on their disposition and/or repair at the end of

the inspection period. (Section M1.4)

2

Maintenance personnel, based on identified drawing discrepancies

with as-built configuration, installed blanks on the Unit 1 and

Unit 2 auxiliary building ventilation system vents supplying the

control battery rooms. Subsequently, it was determined that the

blanks adversely affected the Unit 1 and Unit 2 penetration room

ventilation system (PRVS) tests, and should not have been

installed. A violation was identified to address the failure of

Maintenance personnel to initiate a Problem Investigation Process

Report for problem evaluation when drawing discrepancies were

identified. (Section M4.1)

Maintenance personnel failed to implement the procedural

requirements for restoration of the Main Steam Safety Valves

(MSSV) by not ensuring spindle nut cotter pins were installed on

two Unit 3 MSSVs and improperly installing the cotter pins on four

Unit 2 MSSVs. These examples of poor Maintenance performance

could have led to entry into Emergency Operating Procedures and/or

loss of the steam generators as decay heat removal paths. An

apparent violation with two examples was identified. (Section

M4.2)

Engineering

The licensee's interim corrective actions with respect to a recent

main feedwater pump failure were adequate. (Section E1.1)

A violation was identified concerning an inadequate Letdown

Storage Tank (LDST) Level Calibration Procedure. (Section E8.1)

A non-cited violation was identified to address the inadvertent

removal of redundant power on the Unit 1 and Unit 3 LDST

instrumentation. (Section E1.2)

Plant Support

The licensee effectively implemented a program for shipping

radioactive materials and for classifying waste destined for

burial. (Section R1.1)

The licensee's water chemistry control program for monitoring

primary and secondary water quality had been implemented in

accordance with the TS requirements and the EPRI guidelines for

Pressurized Water Reactor water chemistry. (Section R1.2)

The licensee was maintaining a high level of operability for

radiation monitors in 1996. (Section R2.1)

The transportation training focused on good radiological control

work practices and compliance with transportation regulations.

(Section R5.1)

Enclosure 2

3.

The licensee had complied with the TS required program for

conducting audits of station activities. (Section R7.1)

A non-cited violation was identified for an inadequate procedure

in the Technical Support Center for terminating an Unusual Event.

(Section P3.1)

Enclosure 2

Summary of Plant Status

Report Details

On October 4, 1996, Unit 1 reduced power to fifteen percent and the main

turbine generator was taken offline. The unit remained at fifteen percent

power to provide steam for the shutdown of Unit 3. On October 9, 1996, the

unit was shutdown, and remained in that condition throughout the rest of the

reporting period (Section 01.2).

Unit 2 remained in cold shutdown for the entire reporting period. On October

17, 1996, the licensee entered midloop operation to replace a leaking cold leg

resistance temperature detector (RTD) (Section 01.3).

Unit 3 remained in a refueling mode throughout the entire reporting period.

Review of UFSAR Commitments

While performing inspections discussed in this report, the inspectors reviewed

the applicable portions of the UFSAR that related to the areas inspected. The

inspectors verified that the UFSAR wording was consistent with the observed

plant practices, procedures, and/or parameters.

I. Operations

01

Conduct of Operations

01.1 General Comments (71707)

Using Inspection Procedure 71707, the inspectors conducted frequent

reviews of ongoing plant operations. In general the conduct of

operations was professional and safety-conscious; specific events and

noteworthy observations are detailed in the sections below.

01.2 Unit 1 Shutdown and Rod Drop Test

a. Inspection Scope

On October 9, 1996, the licensee reduced power on Unit 1 from

approximately 15 percent and subsequently tripped the unit. The

licensee manually tripped the unit to perform a rod drop test. The

licensee has a program to check the drop times and evaluate/replace

Control Rod Drive Mechanisms (CRDM) if times exceed a 1.40 second

administrative limit (TS limit is <1.66 seconds). The inspectors

observed the power reduction and the rod drop test.

b. Observations and Findings

The licensee held an effective pre-job briefing on the power reduction

and the rod drop test. Reactor engineers were present to support

performance of the test. Once the evolutions were understood, the

Operations staff cleared the Control Room (CR) of extraneous people and

readied the CR for the test.

2

During the power reduction, all control and parametric indications were

nominal. As power approached the trip test point as described in

procedure PT/1/A/600/15. Control Rod Movement, power reduction was

slowed and control board indications were carefully observed. After the

trip, Operations performed appropriate checks to ensure that all rods

were in the core and the reactor was shutdown.

Reactor engineers determined that the test was valid and that the rod

insertion times, while longer than previous testing times, were well

within the allowed TS limits. Nine of the rods did not drop into the

core in less than the allowed administrative limit. The administrative

limit is used by the licensee to ensure the TS limit is not exceeded.

Management determined that the nine CRDMs would require replacement. In

addition, based on its approach to the 1.40 second administrative drop

time limit, one additional CRDM would also be replaced. The replacement

actions were completed during this period.

c. Conclusions

The Unit 1 power reduction and rod drop test were effectively performed

in a professional and controlled manner.

01.3 Unit 2 Midloop Operation

a. Inspection Scope

The inspector reviewed the Unit 2 midloop operations as controlled by

procedure OP/2/A/1103/11, Draining And Nitrogen Purging Of Reactor

Coolant System.

b. Observations and Findings

During the Unit 2 forced outage, the licensee reduced Reactor Coolant

System (RCS) inventory and reached the midloop operations level on

October 17, 1996. Unit 2 was in midloop status for approximately

eighteen hours. Midloop conditions were required for the replacement of

the 2B1 cold leg RTD which was leaking. The inspectors reviewed the

licensee's controls prior to the reduction of RCS inventory and verified

that the requirements were met while operating at the reduced inventory

levels as specified in procedure OP/2/A/1103/11, Enclosure 3.6.

Requirements for Reducing Reactor Vessel Level to < 50" on LT-5. This

procedure stipulated the sequence and steps required for reduction of

RCS inventory and mid-loop operation. It further specified the

precautions and limitations to be adhered to while in midloop

operations.

The inspector verified that the requirement for two independent trains

of RCS level monitoring was met while at reduced inventory. This was

accomplished through the use of two permanently installed instruments

(LT-5A and LT-5B) and two temporary ultrasonic instruments. During the

Enclosure 2

3

approach to midloop, level reduction was properly delayed because of the

development of ultrasonic instrument problems. The licensee addressed

the problems appropriately. Level indications were displayed in the CR

on the LT-5A and LT-5B indicators, the Inadequate Core Cooling Monitor,

and on the Operator Aid Computer.

The inspector verified that two trains of core exit thermocouples were

available and utilized while at reduced inventory, as well as that the

two sources of inventory makeup and cooling were available for

operation. Multiple sources of offsite power were also available.

c. Conclusion

The licensee implemented and maintained the requirements specified by

procedure while accomplishing reduced inventory operations without

incident. The inspector concluded that the Unit 2 midloop operations

were well controlled and coordinated.

01.4 Cold Weather Preparations

a. Inspection Scope (71714)

The inspector reviewed the licensee's program to protect equipment and

systems against extreme cold weather conditions.

b.

Observations and Findings

The licensee's cold weather protection program was based on an

evaluation of plant equipment where conditions were such that freeze

protection was necessary. The evaluation included plant areas/equipment

that have experienced problems in the past. The more significant areas

included: (1)

the Borated Water Storage Tank (BWST) level indication,

(2)

the Elevated Water Storage Tank (EWST) level indication, and (3)

the

cooling water to the Condenser Circulating Water (CCW) pumps.

On November 15. 1996, the inspectors reviewed the status of heat trace

alarm panels on all three units. Two annunciators were found to be in

the alarm state. However, the affected heaters were not related to

freeze protection and both had been identified by the licensee for

corrective actions. Control room annunciation was periodically reviewed

by the inspectors during routine control room tours. Loss of cooling

water flow to the CCW pumps will actuate a CR alarm.

The inspector verified that freeze protection program actions were

initiated as required when Control Room Alarm, 1SA9B3, RBV Purge Inlet

Temp Low, annunciated indicating outside temperature had reached a low

of 40 degrees F. The program response required that various heaters be

reviewed for malfunctions and steam supplies be readied for use per

OP/0/A/1106/22. Auxiliary Steam System. A second control room alarm

annunciates when the outside temperature drops to 35 degrees F. The

Enclosure 2

4

requirements for that alarm are outlined in Enclosure 5.12, Cold Weather

Checklist, of OP/1/A/1102/20. Shift Turnover. This procedure checklist

specified various preventive measures to be implemented such as building

doors being closed, dampers being closed, heaters being turned on and

verified to be operating properly, proper cooling water flows to outside

equipment, trench covers in place, heat tracing operating properly, and

building heating systems in service. The inspectors toured areas of the

plant, observing damper and door status.

The inspectors reviewed and/or discussed with the licensee the

following:

-

The most recent Work Orders (WO) that were performed on heat

tracing for the BWST level indications [Unit 1, W091037141 (last

performed 2/12/96), Unit 2, W091037410 (last performed 6/5/95),

and Unit 3, W091037645 (last performed 6/12/96)]. These circuits

do not have alarms and a failed heat trace circuit would not be

detected by the operator during heat trace panel checks. However,

redundant level instrumentation is provided and is heat traced.

-

Site discrepancy reports (PIPs 2-96-0252, 0-96-2185, 0-96-2372,

and 0-96-0639) had been generated in reference to problems

experienced at Oconee Nuclear Station (ONS) and other industry

sites. A corporate audit was performed by Duke Power Company (DPC)

to formalize a freeze protection program for all three nuclear

sites. As a result of that audit, Problem Investigation Process

(PIP) report 0-096-0639 was generated to indicate areas that are

not consistent between the Duke facilities.

-

Liquid radiological waste building freeze.protection issues. The

liquid waste building has no steam heat and temporary space

heaters must be maintained to assure proper protection.

-

Procedure upgrades that are planned or being evaluated by site

management for implementation.

Based on the above, the inspectors noted that the licensee had initiated

enhancements in several programmatic areas. Specific changes are still

being pursued by the licensee under the corrective action program. The

inspectors verified that the BWST heat trace instrumentation was

calibrated on its last normal 18 month frequency. Procedures require

that the liquid radiological waste building is manually maintained above

freezing by appointed freeze protection personnel. Additional

programmatic improvements are scheduled in the licensee's corrective

action program.

Enclosure 2

c. Conclusions

The status of plant freeze protection equipment and program was

determined to be adequate. However, the program will be enhanced with

the implementation of actions that have been initiated by the licensee.

02

Operational Status of Facilities and Equipment

02.1 Engineered Safety Feature System Walkdowns (71707)

The inspectors used Inspection Procedure 71707 to walkdown accessible

portions of the following safety-related systems:

Keowee Hydro Station

High Pressure Injection System

Main Steam System

Equipment operability, material condition, and overall housekeeping were

acceptable in all cases. Several minor discrepant conditions were noted

by the inspectors in the Units 1 and 2 Emergency Core Cooling System

(ECCS) pump areas. These were present after an extensive paintout

period in these areas. Examples of the found conditions were bent

instrument lines, taped covers on mechanical joints, and trash in open,

uncovered floor drains. The discrepancies were reported to the licensee.

04

Operator Knowledge and Performance

04.1 Unit 3 Reactor Building Purge System (71707)

On November 12, 1996, alarm 3SA-9, RBV Purge Inlet Temp Low, annunciated

on the Unit 3 Control Room panel. A Non-Licensed Operator (NLO) was

dispatched to the 3B Reactor Building Inlet Purge equipment area to

determine the cause for the alarm. The NLO completed the alarm response

requirements and found no problems. However, the operator noticed that

a damper indicator lever was not in the position that he had remembered

it during previous inspections of that equipment. He opened a duct

panel door and inspected the inside of the duct. As a result, the

operator identified that the inlet dampers had been damaged.

Subsequently, the purge system was shut down for repairs.

The inspectors noted that the NLO aggressively pursued the cause of the

alarm. The Auxiliary Steam system was experiencing problems at that

time and low steam pressure was the most likely suspect for the

annunciated condition since the heating steam was supplied from that

source. The NLO demonstrated excellent operational skills by

understanding the equipment and continuing to investigate the cause of

the problem.

Enclosure 2

6

05

Operator Training and Qualification

05.1 Operator Requalification Program (71001)

a. Inspection Scooe (71001)

During the period of November 12-15, 1996, the inspector used guidance

from Inspection Procedure 71001 to review and evaluate the licensee's

operator requalification program in the area of the Unit 3 Digital

Integrated Control System (ICS) modification training, start-up

training, lesson plan (system description) evaluation, examination

review, operator license disposition and procedural validation.

b. Observations and Findings:

The inspector observed two sessions of a start-up training lab on the

Unit 1 simulator with the Unit 3 digital ICS model installed. The

simulator training crews consisted of four operators. The inspector

observed two of the four operators performing start-up training using

the new digital ICS. The two additional operators were questioned by

the instructor while the start-up lab was being conducted. When the

first group was done with the start-up lab the two groups exchanged

positions. During the start-up training lab the inspector conducted

interviews concerning their training with six operators, two Reactor

Operators and four Senior Reactor Operators. Start-up training is

scheduled to be completed January 2, 1997.

The inspector found that each operator considered the first round of

classroom training adequate in providing technical knowledge concerning

the digital ICS modification. The inspector questioned the operators

concerning the ability to operate both digital and analog ICS models.

The operators stated that they felt it would not be a problem going

between the different ICS models provided some type of "just-in-time"

training was provided prior to assuming the shift on either unit. The

operators interviewed also stated that their opinion on the ability to

operate both the new and old ICSs may change once they became exposed to

the malfunction training scheduled in December. 1996.

The inspector reviewed lesson plan OP-OC-STG-ICS. Integrated Control

System (STG-ICS). The training department provided sixteen hours of

classroom training to plant operators. This training was completed for

all licensed personnel on October 8, 1996. Following this training,

additional ICS review was provided and an examination was prepared for

all licensed personnel.

All licensed operators received the

examination. However, eighteen personnel have to be retested due to

receiving a failing grade. The inspector reviewed one comprehensive ICS

modification examination. The examination contained twenty detailed

multiple choice questions concerning the modification and was found to

adequately test that knowledge.

Enclosure 2

7

The inspector discussed with the Training Department's staff their

recommendation to the Operations Department concerning the dispensation

of current license holders. At the time of the inspection, the Training

Department had not decided on what their recommendation would be

pertaining to licensed operators. The inspector determined that the

Training Department would not make a recommendation until malfunction

training was started, allowing them time to evaluate problem areas not

previously identified. Malfunction training was scheduled for the first

crew during the week of December 2. 1996. Since the results of

malfunction training will be an decision point, this item will be

tracked under Inspector Followup Item (IFI) 50-287/96-16-06, ICS

Malfunction Training Results.

The inspector observed two separate sessions of the validation of

testing procedures. The procedures being evaluated were marked

"Preliminary." The group was comprised of plant engineers, operations

personnel and training instructors. The procedures evaluated were

TN/3/B/2989/00/ALI-26. ICS/NNI Transient Testing at Power, and

TN/3/B/2989/0/A-03. Loss of ICS/NNI Power Testing at 15% Reactor Power.

The inspector observed a good working relationship within this group.

c. Conclusions

The inspector concluded that the first round of start-up training

conducted on the new digital ICS model was satisfactory. The inspector

also concluded that operators felt confident with going from the analog

to the digital ICS, however, the inspector was unable to determine the

actual impact without viewing the malfunction training scheduled in

December. The inspector determined that the sixteen hours of operator

requalification class room training contributed to the confidence

exhibited by the operators during interviews.

By reviewing the system description, the inspector determined that the

new ICS model uses inputs differently than the analog version. The

system description was well written in clear and concise language. This

document was formatted in a logical sequence, which enabled a

comprehensive understanding of a very complex system.

The inspector concluded from the review of one examination that a

comprehensive examination was administered to the operators. The

examination contained pertinent test items. The examination encompassed

a range of aspects concerning the integrated control system.

The inspector concluded the validation process for the testing

procedures was conducted in a professional manner. The validation team

discussed various aspects of the testing scheme while providing insights

concerning certain aspects of plant systems and contingency actions not

addressed in the procedures.

Enclosure 2

8

08

Miscellaneous Operations Issues (92901. 92700)

08.1 (Closed) URI 50-270/96-12-04 Pressurizer Safety Valve 2RC-67

Operability

This item addressed the technical issues associated with pressurizer

safety valve (PSV) 2RC-67 not lifting within the required setpoint. As

documented in PIP 2-096-0945. the early actuation of the 2RC-67 would

delay a reactor trip for transients that trip on high pressure, or the

reactor may trip on a different trip function.

The licensee performed

an analysis on the past operability of 2RC-67, as documented in

calculation OSC-6687. PSV Past Operability Evaluation (PIP #2-096-0945).

The conclusion of OSC-6687 determined that PSVs would have performed

their intended safety function during Cycle 15 based on the licensee's

analysis results. The inspector reviewed OSC-6687 and identified no

problems. This item is closed.

08.2 (Closed) URI 50-270/96-12-03 Delay In Licensee Event Report (LER)

Submittal

This item was opened pending the licensee's results of the past

operability review for PSV 2RC-67. The licensee determined that 2RC-67

was past operable as documented in a letter dated October 10, 1996, from

Duke Power Company to the U.S. Nuclear Regulatory Commission.

Therefore, the licensee determined that the event was not reportable per

10 CFR 50.73. As described above, the inspector reviewed the evaluation

and found no problems. This item is closed.

08.3 (Closed) LER 270/96-03 Pressurizer Relief Valve Technically Inoperable

The licensee determined that this event was not reportable, and that the

LER was not required. During the initial report, the licensee indicated

that PSV 2RC-67 failed to meet its as found set pressure band. After

further analysis, it was concluded that 2RC-67 would have performed its

intended safety function. This item is closed.

Enclosure 2

III

9

II.

Maintenance

M1

Conduct of Maintenance

M1.1 General Comments

a. Inspection Scope (62703, 61726)

The inspectors observed all or portions of the following maintenance

activities:

TN/3/A/0E9360/00 Procedure For The Implementation and

Verification of Minor Modification OEC-9360

(Wet Tap on CCW-42)

WO 96063295

Keowee Unit #1 Turbine Sump Pump's Quarterly

Test

PT/3/A/203/04

Low Pressure Injection System Leakage

MP/0/A/1500/009

Defueling/Refueling Procedure (Unit 3)

WO 96041652

PM Relays In Switchgear 3TD14

WO 95056597

NSM-32976, Replacement of 3HP-5

WO 96084056

Wide Range Instrument Channel Check

WO 96080249

2HD-50 Valve Replacement

WO 95028313

OEC-7451. Replace 1SD-40

WO 96055134

Replace Valve Seat on 3C-20

WO 96081630

PM Valve 2HPSW-85

WO 96079756

NSM 2491, Steam Drain Modifications

WO 96011371

NSM 32979. Replace 2MS-126, 130, and AS-1

WO 96079787

Investigate and Repair 2LPSW-6

b. Observations and Findings

The inspectors found the work performed under these activities to be

professional and thorough. All work observed was performed with the

work package present and in active use. Technicians were experienced

and knowledgeable of their assigned tasks. The inspectors frequently

observed supervisors and system engineers monitoring job progress.

Enclosure 2

10

Quality control personnel were present when required by procedure. When

applicable, appropriate radiation control measures were in place.

c. Conclusion

The inspectors concluded that the maintenance activities listed above

were completed thoroughly and professionally.

IM1.2 Implementation of Temporary Modification to Remove Valve 1LPSW-254

a. Inspection Scope (62707. 40500)

On October 15. engineering personnel performing a visual inspection of

valve 1LPSW-254 identified a crack in the valve stem at the keyway. The

A train of Low Pressure Injection (LPI) was removed from service, and a

temporary modification was initiated to remove the valve from the

system. To implement the modification, the licensee installed a

mechanical plug downstream of valve 1LPSW-254 to provide an isolation

boundary for the work. A temporary modification (TSM 1301) was

developed to remove the valve from the piping system and replace it with

a spacer. This maintenance evolution rendered the A train of LPI unable

to perform its decay heat removal function with the unit in cold

shutdown.

The inspector assessed the maintenance activity by performing the

following:

observation of interdepartmental planning and contingency

meetings: observation of management, operations, and maintenance prejob

briefings; observation of work in progress; review of Temporary

Modification TSM-1301. Temporary Removal of 1LPSW-254 from the Piping

System, including the 10 CFR 50.59 evaluation: review of procedure

TN/1/A/1301/TM/01M, Procedure to Install Temporary Modification TSM

1301: and attendance at Plant Operation Review Committee Meetings on the

subject.

b. Observations and Findings

During the planning of the maintenance evolution, operators identified

enhancements that would improve existing procedures to cope with a loss

of decay heat removal, particularly with the specific plant conditions

that existed at the time the A train was to be isolated. Commencement

of the maintenance was delayed until the enhancements could be

incorporated into the procedures and described in the operations prejob

briefing information.

Management, operations, and maintenance prejob briefings consistently

emphasized the actions that would be necessary in response to a loss of

decay heat removal.

Enclosure 2

11

The temporary modification, its associated 10 CFR 50.59 evaluation, and

implementing procedure were complete, of appropriate detail, and

developed in accordance with station procedures.

The maintenance, including the installation of the mechanical plug

(which was performed by a contractor), was performed in a controlled

manner with an appropriate level of management oversight.

c. Conclusion

Contingency planning for a potential loss of the decay heat removal

function while a single train of LPI was available during maintenance to

remove valve 1LPSW-254 was appropriate. The implementation of the

temporary modification was performed in a controlled manner with an

appropriate level of management oversight.

M1.3 Maintenance Welding (55050)

a. Inspection Scope

The inspector reviewed the control of welding processes and weld

production.

b. Observation and Findings

The inspector determined that the Generation Services Department at

Duke's Corporate Offices was responsible for generating and revising the

Corporate Welding Manual. This department was also responsible for

generating and issuing weld procedure qualifications, welder performance

qualifications, and the code required updates used in the field to

verify welder qualification and work assignments. Welding procedures

and welder performance qualifications were executed to the requirements

of the latest approved edition of ASME Code Sections IX and XI as

applicable.

Welding activities at the ONS are controlled by the

Maintenance Welding Manual (manual), and the applicable construction

code which controls certain fabrication, inspection and testing

requirements for given welds. Mechanical/Civil Equipment Engineering,

generates and revises the manual and administers the welding program at

ONS. The Superintendent of Mechanical Maintenance implements and

maintains control of the welding program. Responsibilities for weld

production and QC inspections are assigned to the Mechanical/Civil

Manager and to the Maintenance Support Manager, respectively.

As required by the welding manual, Class G, non-QA, piping is installed

per the appropriate guidelines with documentation of required

inspections. Production welds in this category are subject to a final

visual inspection that are performed by the welding supervisor or his

designee. Also, Section 9 of the welding manual provided a list of

craft responsibilities and the general requirements to be followed

during weld fabrication.

These included use of appropriate materials,

Enclosure 2

12

Field Weld Data Sheet, weld joint details, cleanliness, cold spring,

preheating and postweld heat treatment.

The inspector identified the following observations which were discussed

with the licensee's cognizant engineer who has been given the

responsibility for reviewing and revising the subject manual as part of

the overall corporate effort to improve the Duke welding program.

Visual inspections of completed welds fabricated to B31.1

requirements are presently performed by the welding supervisor or

his designee. To provide increased independence, this type of

inspection can be done by a welding inspector or QC inspector who

has been trained and qualified in accordance with applicable ANSI

Standards and Duke's written program.

Paragraph 9.6 of the welding manual requires the welder/fitter to

achieve weld fit-up without unacceptable cold spring. No details

or specifics are provided except for the applicable ONS

specification given as reference. The control of cold spring

appears to be a function best monitored by engineering.

Preheating is another responsibility for which welders are

accountable. Paragraph 9.8 states in part that preheating shall

be performed in accordance with the specified Field Weld Data

Sheet (FWDS). The inspector noted that the FWDS states the

requirement for preheat and the appropriate temperature, but does

not identify the procedure which provides the necessary

information for acceptable heat treating practices.

In addition to the above, the inspector reviewed applicable FWDS to be

used for pipe replacement and check valve installation for the first and

second stage reheater drain tanks A and B. FWDS reviewed included

L-350, Rev. 17; L-365, Rev. 4: L-231, Rev. 18; L-250. Rev. 17; and

L-264. Rev. 3. FWDS reviewed were to be used for welding the following

materials:

Mild carbon steel to like material

Mild carbon steel to stainless steel material

Stainless steel to like material

The welding processes to be used for joining these materials were

shielded metal arc and gas tungsten arc or a combination of the two.

The inspector's review revealed that these procedures were properly

qualified and documented in accordance applicable code requirements.

Pipe and Valve Installation - Reheater Drain Line Modification

The instructions and documentation for installation of pipe and valves

in the reheater drain system of Unit 2 are described in modification NSM

22941, Part AM1 and Temporary Modification Procedure TN/2/A/2941/0/AM1.

Enclosure 2

13

Enclosure 5.4 of the package will be used for instructions and

documentation of new pressure retaining welds. Also, the instructions

provide for QC/ANI inspections, and associated hold points and for

surfaces examinations of root and completed welds. Additionally,

cleanliness requirement for carbon and stainless steel piping as

recommended by ANSI Standard N45.2.1-73 were added as a quality measure.

Field Inspections

As documented previously in Inspection Report 50-269,270.287/96-15.

extensive field inspections were performed by the licensee and

contractors focusing on locating branch connections, taking data, and

performing calculations to determine whether as built conditions met

minimum code requirements. Branch connections that failed to meet code

requirements were scheduled for replacement. Additionally, pipe and

elbow welds whose location could have rendered them subject to cracking

in the weldment or associ.ated base metal were radiographed to determine

their integrity. Selected pipe and elbow welds were visually examined

for anomalies. Associated surfaces were examined using a magnetic

particle examination technique to look for evidence of crack

indications. Finally, a consultant was contracted to perform field

inspections and to provide stress analysis evaluations with respect to

the effects of water hammer on existing piping.

c. Conclusion

The licensee's welding instruction and field inspection appeared

appropriate. The licensee's efforts to identify and document field

conditions following the Unit 2 water hammer event were commensurate

with applicable code requirements and quality standards, and reflected a

conservative attitude.

M1.4 Inservice Inspection Unit 3 (73753)

a. Inspection Scope

Observe inservice activities to determine adequacy of nondestructive

examination and compliance with code requirements and FSAR commitments.

b. Observation and Findings

The scheduled Unit 3 refueling outage was changed to coincide with the

unscheduled shutdown in response to the water hammer events on Unit 2.

This outage was identified as End-Of-Cycle 16 (EOC-16) and was the

second refueling of the third interval since commercial plant operation.

The applicable code was identified as ASME Sections XI and V. 1989

Editions. The scope of the Inservice Inspections (ISI) during this

outage was limited to: augmented examinations in response to IE Bulletin

88-08; and followup ultrasonic examinations in response to previously

identified rejectable indications in welds No. 3SGA-WG8-1 and 3SGA-WG8-2

Enclosure 2

14

of Once Through Steam Generator (OTSG) "A"

of Unit 3. Thi-s item was

documented in PIP No. 3-092-0371 for tracking purposes. In addition,

inspections included examination of the pressurizer relief nozzle welds,

pressurizer spray nozzle weld and upper head and upper shell course

weld.

The inspector observed the examination of the aforementioned welds on

the pressurizer. This included system calibration and examination with

00, 450 and 600 transducers. Duke Non-Destructive Examination (NDE)

procedures used for these examinations included NDE-640, Rev. 1, for the

00 scan and NDE-620, Rev. 5, for the 450 and 600 scans.

These procedures have been reviewed on previous inspections and were

found to meet code requirements. Calibrations and examinations were

properly performed and documented. Indications were evaluated and

dispositioned. Limited examinations were calculated and percentage of

weld examination/coverage was documented. Personnel who performed the

examinations were adequately trained and knowledgeable of code and

procedural requirements. Rejectable indications were not identified.

Eddy Current Examination of Unit 3 OTSGs

The scope of examining OTSG tubes at ONS Unit 3 during the current

refueling outage (EOC-16) was as follows:

(1) Inspect 100% of inconel-600 plugs and 40% of inconel-690 plugs on

the hot leg, using motorized pancake coil (MRPC) probe.

(2) Inspect Lane/Wedge tubes in hot leg of both OTSGs with MRPC.

(3) Inspect selected inconel-600 and -690 sleeves in hot leg of both

OTSGs with Bobbin and Plus-Point coil probes.

(4) Inspect 100% of tubes available in both OTSGs with Bobbin coil

probe.

(5) Inspect roll transitions in hot leg of both OTSGs with MRPC coil

probe.

With respect to item (5)

above, a 20% randomly selected sample was

scheduled for examination with MRPC coil probe. The sample was

subsequently increased to 100% when the examination identified an

indication in the roll transition region. This indication was believed

to be associated with Primary Water Stress Corrosion Cracking (PWSCC)

mechanism.

The licensee plans to pull four tubes for a metallurgical examination to

determine conditions associated with tube degradation. Procedures used

to perform the examination and analyze results comply with ASME Code

Enclosure 2

15

Section XI. 1989 Edition with no Addenda. Also applicable by reference

is Regulatory Guide 1.83. July 1975. Applicable procedures include:

NDE-701. Rev. 3:

Multifrequency Eddy Current Examination of

Steam Generator tubing at McGuire, Catawba

and Oconee Nuclear Stations.

NDE-707. Rev. 3:

Multifrequency Eddy Current Examination on

Non-Ferrous Tubing, sleeves and plugs

using a motorized rotating coil probe.

In addition to these procedures, the licensee developed a set of

guidelines which are used to assist in data acquisition and analysis of

data at the Oconee Nuclear Station and to establish consistency and

compliance with applicable requirements. These guidelines were as

follows:

Eddy Current Acquisition Guidelines, October 6. 1996

Eddy Current Analysis Guidelines, October 9, 1996

Data acquisition was being performed by the licensee using Zetec's

Eddynet Acquisition system. Data analysis was being performed offsite

at the McGuire Nuclear Station, as well as Framatome in Lynchburg, VA

and Rockbridge, IL.

At the close of this inspection on October 18, 1996, bobbin coil

examination was in progress, but had not reached the point of

identifying tubes for plugging. In a similar manner, examination of the

roll transition at the upper tube sheet was making good progress, but no

evidence of PWSCC had been identified. On October 22, 1996, the

licensee's accountable engineer indicated that preliminary evaluation

identified three tubes in OTSG "B"

with axial indications. The suspect

tubes were identified in locations 136-47, 113-114. and 132-1. The

licensee expected to have the examination and the list of tubes to be

repaired during the week of October 27, 1996.

c. Conclusion

ISI examinations scheduled for this outage were being performed as

required by well trained personnel following procedures written in

compliance with applicable code requirements. Personnel performing the

inspections were well qualified to execute their assigned tasks. Eddy

current examinations were consistent with Technical Specifications 4.17

requirements. Three tubes were identified in S/G "B"

with PWSCC

indications in the roll transition region of the upper tubesheet. No

decisions had been reached on their disposition and/or repair at the

close of the inspection period.

Enclosure 2

16

M4

Maintenance Staff Knowledge and Performance (92902. 62707)

M4.1 Failure To Initiate a PIP

a. Inspection Scope

The inspector reviewed an issue involving the installation of blanks on

the auxiliary building ventilation system (ABVS) supply vents which feed

the Unit 1 and Unit 2 control battery rooms. The blanks adversely

affected the Unit 2 and Unit 1 Penetration Room Ventilation System

(PRVS) testing.

b. Observations and Findings

On October 2, 1996. during the performance of PT/2/A/0100/010.

Penetration Room Ventilation System Vacuum Test, the PRVS could not

maintain a vacuum against the Unit 2 control battery room as documented

in PIP 0-096-1960. The licensee determined that Maintenance personnel

had installed blanks on the ABVS supply vents feeding the Unit 2 control

battery room on September 25, 1996, which adversely affected the PRVS

test. On October 9, 1996, the licensee performed PT/1/A/0100/010,

Penetration Room Ventilation System Vacuum Test, and the system could

not maintain a vacuum against the Unit 1 control battery room. Blanks

had also been installed on the ABVS vents feeding the Unit 1 control

battery room on September 25. 1996. Isolating the supply air to the

battery rooms reduced the pressure in the rooms to the point where it

was no longer positive with respect to the penetration room when the

PRVS was in operation. The licensee determined that there were no

present operability concerns on Unit 1 and Unit 2 since they were

shutdown. The Unit 1 past operability evaluation documented in OSC

6679. Penetration Room Allowable Leakage, concluded that the Unit 1 PRVS

was past operable from September 25. 1996. through October 9, 1996. The

licensee determined that there was no past operability concern for Unit

2 because the blanks were installed while the unit was offline. The

inspector noted that there is an open deviation (DEV) on the operability

of the PRVS (DEV 50-269.270,287/94-24-04).

The licensee incorporated minor modification ONOE-9540 which removed the

installed blanks from Unit 1 and 2 ABVS supply vents in the control

battery rooms. The inspector independently verified that the blanks had

been removed from the supply vents. The modification will also revise

the drawings to reflect the correct as-built configuration (blanks

removed). The licensee successfully performed the Unit 1 and Unit 2

PRVS tests after the implementation of ONOE-9540.

In early September 1996. Maintenance personnel identified that station

drawings 0-504A and 0-2504B indicated that the subject vents should have

been blanked off. The NSM which originally installed the Control

Battery Room Air Conditioning Units was also intended to blank off the

ABVS supply vents in the rooms. Maintenance initiated work requests

Enclosure 2

17

(WR) 96038038 and 96037440 to install the blanks to assist cooling the

battery rooms during the summer since the air temperature coming out of

the duct was higher than the 80 degree limit for the room. Nuclear

Station Directive (NSD) 208. Problem Investigation Process. provides

criteria for initiating a PIP for drawing discrepancies. On September

9, 1996, Maintenance personnel identified that drawing 0-2504B did not

match as-built conditions, but failed to initiate a PIP as required by

NSD 208. The inspector concluded that Maintenance personnel should have

initiated a PIP once the drawing discrepancies were identified, then

Engineering could have evaluated the installation of the blanks. This is

being identified as example one of Violation 50-269,270/96-16-01,

Maintenance Failed To Initiate a PIP. On September 12, 1996,

Maintenance personnel identified that drawing 0-504A did not match as

built conditions, but again failed to initiate a PIP. This is being

identified as example two of Violation 50-269,270/96-16-01. Maintenance

Failed To Initiate a PIP.

c. Conclusion

A violation with two examples was identified to address the failure of

Maintenance personnel to initiate a PIP to address drawing discrepancies

on the missing blanks on the ABVS vents supplying the Unit 1 and Unit 2

control battery rooms. Maintenance initiated WRs that installed blanks

on ABVS supply vents which adversely affected the Unit 1 and Unit 2 PRVS

testing.

M4.2 Main Steam Safety Valve (MSSV) Cotter Pin Inspection (92902, 40500)

a. Inspection Scope

In May 1996, another B&W plant had a Dresser Main Steam Safety Valve

(MSSV) fail to reseat after lifting. This was due to its spindle nut

not being held in place by a cotter pin that should have engaged a slot

in the nut and a drilled hole in the valve's spindle. The nut vibrated

down the spindle and interfered with the valve's downward motion as the

lifted. That B&W plant had Main Steam Isolation Valves and a Feed-Only

Good-Generator system. As documented in Inspection Report 50

269,270,287/96-12, the licensee was aware of the problem and determined

that the specific problem was not an immediate concern at Oconee

because: the Oconee valve vendor was a different manufacturer (Crosby

Valve and Gage Company): the valve details. though similar in function,

were sufficiently different: the Oconee valve procedure specifics would

tend to prevent incorrect cotter pin/nut engagement; and discussions

with valve assembly technicians provided no negative findings. Based on

this and personnel safety concerns while at power, inspection of the 48

MSSVs (8 per steam line; 16 per unit) was scheduled for the next cold

shutdown periods. During recent plant shutdowns to cold conditions for

other reasons, the inspectors participated in the inspections and

reviewed applicable WOs and PIPs.

Enclosure 2

b. Observations and Findings

18

On October 15, 1996, per WO 96080355, the licensee conducted the Unit 1

inspection and did not identify any problems. On October 14, 1996, per

WO 96080322, the licensee conducted the Unit 2 inspection which

identified that spindle nut cotter pins were improperly installed on

four MSSVs. The four MSSVs were 2MS-0001. 2MS-0005, 2MS-0013, and 2MS

0014. Each valve has a nominal lift setpoint of 1100 psig except for

2MS-001, which has a setpoint of 1104 psig. The cotter pins were not

bent sufficiently, and could have vibrated out of the spindle nut. The

subject MSSVs were located on separate steamline headers; therefore, if

the valves failed to reseat under certain conditions both OTSGs could

have been lost as decay heat removal paths. On October 21, the licensee

performed a past operability evaluation for the four MSSVs. It was

concluded that the valves would have performed their protection function

by opening, but the valves could not be credited for closing to provide

a fission barrier and preventing a loss of inventory. The evaluation

also concluded that even if the four valves failed to reseat, the

radiological dose released would not have exceeded the 10 CFR Part 100

limits. This conclusion was drawn assuming a Chapter 15 Steam Generator

Tube Rupture.

The Unit 3 inspection conducted on October 24, 1996, by the inspectors

along with the licensee identified that cotter pins were not installed

on two MSSVs. The two valves were 3MS-0010 and 3MS-0001, each with a

nominal lift setpoint of 1065 psig and 1104 psig, respectively. The

valves were on separate steamline headers; therefore, if the valves

failed to reseat under certain conditions both OTSGs could have been

lost as decay heat removal paths. The licensee's system operability

evaluation concerning the two valves was not available prior to the end

of the inspection period.

On October 29, 1996, the licensee made a 10CFR 50.72 notification

concerning the two Unit 3 MSSVs missing their cotter pins. The licensee

determined that the possibility existed for flow induced vibration to

have caused the unsecured spindle nut to rotate down the spindle toward

the valve body. Therefore, 3MS-0001 and 3MS-0010 could have been

prevented from properly closing, resulting in an potential primary

system overcooling event. On October 30, 1996, the licensee made a

similar 10 CFR 50.72 notification addressing the four Unit 2 MSSVs

having improperly installed cotter pins. The 10 CFR 50.72 section cited

in the reports was "Any event or condition that alone could have

prevented the fulfillment of the safety function of structures or

systems that are needed to mitigate the consequences of an accident".

During each Unit's respective refueling outage the valves were partially

disassembled to perform setpoint tests. The manual lift linkage

assembly, which includes the spindle nut, was removed and re-installed

each time. The licensee considered the parts removed as not being

Enclosure 2

19

safety parts. As reported by the licensee, the Unit 2 valves identified

above did not lift (as expected) during the last reactor trip.

The cotter pins on the four Unit 2 MSSVs (2MS-0001. 2MS-0005, 2MS-0013,

and 2MS-0014) were improperly installed on May 4-5, 1996. Associated

Maintenance Procedure MP/0/A/1200/089, Valve - Main Steam Safety

Setpoint Test, Step 12.3 states that, "Spindle nut cotter pins are in

place and in good mechanical condition." The inspector noted that there

was no documented QC or second party verification to ensure correct

cotter pin installation. The failure of Maintenance personnel to

properly install the subject cotter pins per MP/0/A/1200/089 is

considered a violation of TS 6.4.1 and is identified as example one of

Apparent Violation (EEI) 50-270,287/96-16-05: Failure to Properly

Install MSSV Spindle Nut Cotter Pins.

The two Unit 3 MSSVs (3MS-0001 and 3MS-0010) which had missing cotter

pins should have had the pins installed during the performance of

MP/0/A/1200/089 on July 17-18, 1996. The failure of Maintenance

personnel to properly install the subject cotter pins per

MP/0/A/1200/089 is considered a violation of TS 6.4.1 and is identified

as example two of Apparent Violation (EEI) 50-270,287/96-16-05:

Failure

to Properly Install MSSV Spindle Nut Cotter Pins.

The licensee's proposed corrective action was to perform minor

modifications on all three units' MSSVs to remove the lift lever

assembly (i.e., lift lever, lever pin, lever cotter pin, forked lever,

forked lever pin, forked lever cotter pin, spindle nut, and spindle nut

cotter pin).

The inspector verified that W096083643, W096083248, and WO 96083850 were being generated, and will be implemented during the

ongoing outages. The inspector also reviewed the safety evaluations

associated with the lift lever assemblies and did not identify any

additional issues of concern.

c. Conclusion

Maintenance personnel failed to appropriately implement the procedure

requirements for restoration of the MSSVs by ensuring that cotter pins

were properly installed on two Unit 3 MSSVs and four Unit 2 MSSVs.

These examples of poor Maintenance performance could have led to entry

into Emergency Operating Procedures and/or loss of OTSGs as decay heat

removal paths. Accordingly, an Apparent Violation with two examples was

identified.

M8

Miscellaneous Maintenance Issues (92903)

M8.1

(Closed) IFI 269,270.287/96-12-01 MSSV Cotter Pin Inspection

This item is closed based on the information provided in Section M4.2 of

this inspection report.

Enclosure 2

20

M8.2

(Open) Unresolved Item 269/96-04-04 Root Cause Assessment of Failures

to Valves 1MS-77 and 1LPSW-254

One of the two issues addressed by this item involved unreliability of

valve 1LPSW-254. The valve is in the Low Pressure Service Water (LPSW)

system and is the Unit 1 Train A Low Pressure Injection (LPI) Cooler

outlet isolation valve. Valve 1LPSW-251 is the LPI cooler outlet flow

control and is located directly upstream of 1LPSW-254. As documented in

NRC Inspection Report 50-269,270,287/96-04. piping vibration in the

vicinity of these valves has caused failures of valve 1LPSW-254 in the

past. A modification was implemented in 1992 in an attempt to improve

reliability: however, there have been subsequent failures. Each train

of LPI on all three units has a similar arrangement. The unresolved

item was opened pending the licensee's evaluation of the vibration

problem and determination of necessary corrective actions.

During this inspection period, the A train of LPI was placed in service

for decay heat removal following shutdown of Unit 1. In service

inspections of the valve were performed by engineering personnel. As

documented in PIP 1-096-2000. on October 11 slight motion of the 1LPSW

254 valve stem relative to the operator was identified. On October 12

corrective maintenance was performed to replace the key (which showed

signs of wear) and the operator was rotated 1800 to utilize the unused

keyway in the operator drive sleeve. The A train of LPI was returned to

service following testing later the same day. On October 15, a followup

inspection of the valve by engineering personnel identified a crack in

the valve stem at the key way. The A train of LPI was removed from

service and a temporary modification was initiated to remove the valve

from the system. The inspector observed the work to implement the

modification as documented in Section M1.2. of this report.

Since unreliability of valve 1LPSW-254 continued, the inspector reviewed

the status of Unresolved Item 269/96-04-04. The licensee had completed

the engineering evaluation of the system vibration in the vicinity of

the LPI cooler flow control valves, including an initial recommendation

for corrective action.

The results of the vibration evaluation were documented in an

engineering memo to file dated October 1, 1996. The evaluation

indicated that excessive vibration existed in the LPSW LPI cooler flow

control valves on all three units. The vibration is the result of flow

induced cavitation through the flow control valves. Valve 1LPSW-254 is

the shortest distance downstream from its associated flow control valve.

This has likely contributed to its higher rate of failure. The

engineering evaluation recommended replacement of the flow control

valves with larger valves that included a flow attenuator and the

replacement of the isolation valves with larger valves of the same

style.

Enclosure 2

21

Additional corrective actions for the 1 LPSW-264 failures are still

under review by station management. The failure of 1MS-77 was not

reviewed. The URI .remains open.

III. Engineering

El

Conduct of Engineering

E1.1 3B Main Feedwater Pump (MFP) Gear Failure

a. Inspection Scope

The inspector reviewed the licensee's root cause evaluation and PIPs

associated with the 3B MFP failure which occurred on August 24. 1996.

b. Observations and Findings

On August 24. 1996. Unit 3 experienced a runback to 65% power due to a

loss of the 3B MFP. The licensee determined that the runback was caused

by a failure of the 3B MFP turbine main shaft oil pump (MSOP) to

function because of the failure of the number three and number four gear

set. The actual root cause of the gear failures is still under

evaluation. As documented in PIP 3-096-1626. part of the assessment of

the failure addressed whether the failed gears were a matched pair, or

not. Previous failures dating back to 1994 had identified this as a

problem. The licensee's investigation revealed that the gears that were

replaced were a matched pair but that it was fortuitous and not because

of corrective actions from previous events. PIP 2-094-474 provided

guidance to purchase the gears in matched sets. Due to a lack of

communication, the gears that were already purchased were not returned,

and no matched pairs were ever ordered. Currently, there is an active

purchase identification number for matched gear sets.

Since the late 1980s the licensee had performed major Preventive

Maintenance (PM) on the MFPs every refueling outage (RFO). On October

4, 1994, the licensee changed the major PM to every third RFO and minor

PM to every RFO. On July 25, 1995, the licensee changed the major PM to

every fourth RFO to coincide with MFP rebuild. After this latest

failure, the licensee revised the PM frequency on the MFP front standard

hydraulic system to once per refueling outage until a cost benefit

analysis can be performed on the available MSOP reliability improvement

options.

The inspectors observed the 3B MFP being rebuilt with the new gears.

The licensee conducted the work with appropriate WOs and procedures.

c. Conclusion

The licensee's corrective actions were appropriate to address this

issue.

Enclosure 2

22

E1.2 Letdown Storage Tank Level Redundant Power SuDly

a. Inspection Scope (37551)

The inspector reviewed the circumstances leading to the identification

that the Letdown Storage Tank (LDST) level instrumentation was not

powered from a redundant power supply.

b. Observations and Findings

On October 28, 1996. the licensee identified that Unit 3 LDST level

transmitter ON3HPILTOO33P1 was not powered from the Integrated Control

System (ICS) Redundant Power Panel.

Further investigation revealed that

Unit 1 was also not powered from the Redundant Power Panel.

A modification,.NSM 1.2,3 2728 had been implemented in the 1989 and 1990

time period which changed the transmitters from Bailey to Rosemount

types. During the modification, the redundant power supply detailed on

drawings had not been reconnected on Units 1 and 3, but was properly

installed on the Unit 2 instruments. IP/O/A/0202/1F, HPI LDST Level

Instrument Calibration Procedure, was performed as a post modification

test. The test did not address the redundant power supply.

The inspectors reviewed applicable Bailey Meter Company instrument

drawing D80323245, Rev. DQ (drawing referenced the Rosemount

Instruments) and verified that the field installation was not in

accordance with the drawing.

The consequences of a power failure to

the LDST Level instrumentation was discussed with the system engineer.

A power failure to the instrument would result in the indication

dropping to mid-scale. This mid-scale instrument failure would be less

noticeable than a failure to the low-end of the scale. However, in

reviewing the control room indication, it was learned that there was a

light on the face of the gage which would go out if power failed. It

was further observed that the normal operating range was at

approximately 90 percent of full scale and a failure to the 50 percent

position should be detected by the operators. The inspector concluded

that should the single power source fail, Operations would have detected

the failure within a short period of time.

The licensee issued PIP 0-96-2165 to describe and resolve this problem.

Additionally, they aggressively initiated corrective action. The

licensee has reconnected the redundant power supply on Unit 1

instruments and has scheduled the work on Unit 3 to be performed prior

to its restart. The inspector reviewed the Unit 1 re-installation

functional test data and had no further concerns.

c. Conclusion

Although the LDST indication is not considered safety-related, the

indication is essential (importatant to safety) to ensure that the plant

Enclosure 2

23

is operated in a safe manner. Failure to maintain plant configuration

as detailed on the drawings is a violation. This licensee identified

and corrected violation is being treated as a Non-Cited Violation (NCV),

consistent with Section VII.B.1 of the NRC Enforcement Policy. This

issue will be identified as NCV 269,287/96-16-04, Failure to Maintain

Equipment in Accordance with Plant Drawings.

E8

Miscellaneous Engineering Issues (92903)

E8.1 (Closed) Unresolved Item (URI) 50-269.270,287/96-12-02 LDST Pressure

Level Curves

The licensee determined that LDST level calibration procedure

IP/0/B/0202/001F. Letdown Storage Tank Level vs. Pressure Curve Limits,

did not properly account for instrument uncertainties. The procedure

was in error because a specific gravity correction factor had been

misapplied in calculation OSC-4506, Letdown Storage Tank Level

Instrument Loop Accuracy Calculation For 1, 2. 3 HPILTOO33P1 and 33P2.

The inspector concluded that calibration procedure IP/0/B/0202/001F was

inadequate, in that it did not correctly account for instrument

uncertainties, and is being identified as Violation 50-296.270,287/96

16-02. LDST Calibration Procedure In Error.

As described in IR 50-269.270,287/96-12, there was no present

operability concern. The inspector reviewed calculation OSC-6646. Past

Operability Determination For PIPs 0-096-1539 and 0-096-1550, LDST Curve

Analysis. Calculation OSC-4616 determined the curves for operations use

in maintaining the correct level pressure relationship in the LDST to

ensure that gas would not be carried into the suction of the HPI pumps.

Non-conservatisms were noted in OSC-4616. Specifically, the partial

pressures of gas and water vapor had not been considered in the

calculation. OSC-6646 examined the results of OSC-4616 and previous

revisions of the curves that had been used at ONS. The results of this

calculation were that all points, except one at 92 inches (outside the

normal operating range), were bounded by the data sheets of the previous

calculations. The calculation concluded that there were some extremely

remote conditions (i.e., elevated BWST temperature) that may not have

been bounded. However these conditions were considered not to be

credible. Accordingly, URI 50-269.270,287/96-12-02 is closed.

IV.Plant Support Areas:

R1

Radiological Protection and Chemistry (RP&C) Controls (71750)

R1.1 Transportation of Radioactive Materials

a. Inspection Scope (86750. T12515/133)

The inspectors evaluated the licensee's transportation of radioactive

materials program for implementing the revised Department of

Enclosure 2

24

Transportation (DOT) and NRC transportation regulations for shipment of

radioactive materials as required by 10 Code of Federal Regulations

(CFR) Part 71 and 49 CFR Parts 100 through 177.

b. Observations and Findings

The inspectors reviewed procedures and determined that they adequately

addressed: assuring that the receiver has a license to receive the

material being shipped; assigning the form, quantity type, and proper

shipping name of the material to be shipped; classifying waste destined

for burial: selecting the type of package required: labeling and marking

the package; placarding the vehicle; assuring that the radiation and

contamination limits are met; and preparing shipping papers.

The inspectors reviewed the licensee's records for 15 shipments of

radioactive material and determined the shipping papers contained the

required information. The licensee was maintaining records of shipments

of licensed material for a period of three years after shipment as

required by 10 CFR 71.91(a). Certificates of Compliance (CoC) for the

shipping casks the licensee currently used were reviewed and the

inspectors determined that the CoCs were currently NRC approved for use.

A review of the licensee's computer software for classifying waste

shipments indicated that it had been updated to reflect the latest DOT

isotopic concentration changes in the Al and A2 shipping table values.

c. Conclusions

Based on the above reviews, it was concluded that the licensee had

effectively implemented a program for transporting radioactive materials

and for classifying waste destined for burial.

R1.2 Water Chemistry Controls

a. Inspection Scope (84750)

The inspectors reviewed implementation of selected elements of the

licensee's water chemistry control program for monitoring primary and

secondary water quality. The review included examination of program

guidance, as well as implementing procedures and analytical results for

selected chemistry parameters.

b. Observations and Findings

The inspectors reviewed Technical Specification (TS) 4.1.3. which

described the operational and surveillance requirements for reactor

coolant activity and chemistry. The inspector also reviewed Final

Safety Analysis Report (FSAR) Sections 5.2.1.7 and 9.3.1.2, which

indicated guidelines for maintaining reactor coolant and feedwater

quality that were derived from vendor recommendations and the current

Enclosure 2

25

revisions of the Electric Power Research Institute (EPRI)- Pressurized

Water Reactor (PWR) Primary and Secondary Water Chemistry Guidelines.

The FSAR also indicated that detailed operating specifications for the

chemistry of those systems were addressed in the Chemistry Section

Manual.

The inspector reviewed selected analytical results recorded for Units

1, 2, and 3 reactor coolant and secondary samples taken during June 1,

1996, and October 19, 1996. The selected parameters reviewed for

primary chemistry included pH, dissolved oxygen, chloride, fluoride, and

sulfate. The selected parameters reviewed for secondary chemistry

included pH, dissolved oxygen, fluoride, and chloride. Those primary

and secondary parameters reviewed were maintained well within the

relevant TS.limits and within the EPRI guidelines for power operations

and cold shutdown modes for PWR primary water chemistry.

c. Conclusions

Based on the above reviews, it was concluded that the licensee's water

chemistry control program for monitoring primary and secondary water

quality had been implemented in accordance with the TS requirements and

the EPRI guidelines for PWR water chemistry.

R2

Status of Radiation Protection Facilities and Equipment

R2.1 Process and Effluent Radiation Monitors

a. Inspection Scope (84750)

The inspectors reviewed selected licensee procedures and records for

required surveillances on process and effluent radiation monitors and

for radiation monitor availability.

b. Observations and Findinqs

The inspectors toured the facility and observed the physical operation

of radiation monitors in use. Radiation monitor local digital displays

were compared to control room monitor displays for ten radiation monitor

displays. The displays were determined to be tracking consistently with

each other. The inspectors also reviewed selected surveillance

procedures and records for performance of channel checks, source checks,

channel calibrations, and channel operational tests for the radiation

monitors listed below:

RIA-39

Control room ventilation monitor

RIA-41

Spent fuel building ventilation monitor

3RIA-41

Spent fuel building ventilation monitor

CRIA-43

Unit 1 ventilation monitors

1RIA-44

Unit 1 ventilation monitors

1RIA-45

Unit 1 ventilation monitors

Enclosure 2

26

1RIA-46

Unit 1 ventilation monitors

1RIA-47

Reactor building airborne monitoring system

1RIA-48

Reactor building airborne monitoring system

1RIA-49

Reactor building airborne monitoring system

1RIA-49A

Reactor building airborne monitoring system

Surveillance testing was required by the TSs and/or the Offsite Dose

Calculation Manual (ODCM) to demonstrate that the instrumentation was

operable. Records indicated that the surveillances were current and had

been performed in accordance with the applicable procedures. The most

recent system status report available, which covered the period January

through June 1996, indicated that the overall availability for the

Radiation Monitoring System remained above 99 percent. The inspectors

discussed operability trending methods for both safety-related and

nonsafety-related monitors with the radiation monitor system engineer in

addition to reviewing spare parts inventory data. Operability records

reviewed and discussed with cognizant licensee personnel indicated that

one containment high range monitor had previously been out of service

for a period of 25 days as a result of spare parts availability

problems.

c. Conclusions

Based on the above reviews, it was concluded that the licensee had

effectively implemented procedures to track the availability of

radiation monitors and to demonstrate operability of process and

effluent radiation monitors by performance of surveil ances at the

frequencies specified in the TSs and the ODCM. Discussions with

cognizant licensee personnel and a review of performance records

determined the licensee was maintaining an overall high level of

operability for radiation monitors in the first six months of 1996.

R5

Staff Training and Qualification in Radiation Protection and Chemistry

R5.1 Training for Transportation of Radioactive Material

a. Inspection Scope (86750, TI 2515/133)

The inspectors reviewed training for personnel and supervisors involved

in transportation of radioactive material.

b. Observations and Findings

The inspector reviewed licensee training records and verified that

personnel involved with radioactive material shipping were maintaining

current hazardous material (HAZMAT) training qualifications.

Enclosure 2

27

c. Conclusions

The inspectors determined the licensee's training program associated

with transportation of radioactive material was adequate. The

inspectors concluded the transportation training focused on good

radiological control work practices and compliance with transportation

regulations.

R7

Quality Assurance in Radiation Protection and Chemistry Activities

R7.1 Review of RP&C Self-Assessment Activities

a. Inspection Scope (84750, 86750, TI 2515/133)

The inspectors reviewed a licensee self-assessment and discussed issues

identified with licensee management to determine if the licensee was

identifying issues of substance, proposing corrective actions, and

tracking items for completion in the areas inspected.

b. Observations and Findings

The assessment, Regulatory Audit SA-96-39(ON)(RA), dated August 27,

1996, was conducted during the period of July 22, 1996, through July 30,

1996. at the Oconee Nuclear Site. The scope of the assessment was in

the areas of chemistry, radiation protection, and transportation of

radioactive material program activities. A number of substantive issues

were identified by the audits and were characterized as either findings.

followup items, strengths, weaknesses, recommendations, or observations.

Pursuant to the licensee's auditing procedures, the identified issues,

including corrective actions for the findings, were tracked for

completion of warranted followup actions by initiating PIPs. The

inspector determined that the audits were of sufficient scope and depth

to identify existing problems and that corrective actions for the

identified findings were documented and resolved through the PIP. The

audit results were well documented and reported to facility management

in a timely manner.

c. Conclusions

Based on the above reviews, it was concluded that the licensee had

complied with the TS required program for conducting assessments of

station activities.

Enclosure 2

28

P3

Emergency Preparedness Procedures and Documentation.

P3.1 Emeroency Preparedness Followup to Licensee Event (Unit 2)

a. Inspection Scope (71750)

The inspectors reviewed the declaration and termination actions taken by

the licensee for the licensee's Notice of an Unusual Event (NOUE)

associated with a Unit 2 secondary side steam line break to verify the

licensee complied with their Emergency Coordinator procedures for event

classification.

b. Observations and Findings

The inspectors verified the event was classified in accordance with

licensee procedure RP/O/B/1000/01, Emergency Classification, Change 3,

dated July 16, 1996. The licensee classified this event as an Unusual

Event based on emergency action levels (EALs) identified in the

procedure.

The Event Notification form reviewed by the inspectors, verified the

event was declared and terminated at 8:40 p.m. on September 24, 1996,

from the Technical Support Center (TSC). During the event debrief, the

licensee identified that the Emergency Coordinator procedure did not

contain adequate guidance for event declarations and termination.

Specifically, an event checklist used in the Control Room and Emergency

Operating Facility (EOF) for terminating an event was not available in

the TSC Emergency Coordinator procedure. The licensee initiated a

Problem Investigation Process (PIP) report to evaluate the problem and

completed a procedural revision for the Emergency Coordinator TSC

procedure to provide procedural guidance for terminating a NOUE

consistent with the guidance in the control room and EOF procedures.

The inspector had also identified that the procedure used in the TSC

during the event was not adequate for terminating an Unusual Event. The

inspector informed the licensee that this was a violation of TS 6.4.1

which required written procedures with appropriate instructions and

check-off list shall be provided. The inspector noted that the licensee

took immediate corrective actions to upgrade the TSC procedure. This

licensee-identified and corrected violation is being treated as a Non

Cited Violation, consistent with Section VII.B.1 of the NRC Enforcement

Policy. This issue is identified as NCV 50-269,270.287/96-16-03,

Failure to Provide Adequate Procedural Guidance in the TSC for Exiting a

NOUE.

c. Conclusions

Based on an independent review of records, logs, and interviews with

personnel involved with the event, the inspectors verified the event was

classified in accordance with licensee procedures.

However, the

licensee terminated the event without adequate procedural guidance in

the TSC. Accordingly, an NCV was identified for this licensee

identified violation.

Enclosure 2

29

X1.

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee

management at the conclusion of the inspection on November 20, 1996. The

licensee acknowledged the findings presented.

The inspectors asked the licensee whether any materials examined during the

inspection should be considered proprietary. No proprietary information was

identified.

Partial List of Persons Contacted

Licensee

B. Peele, Station Manager

E. Burchfield. Regulatory Compliance Manager

D. Coyle. Systems Engineering Manager

T. Curtis, Operations Manager

J. Davis. Engineering Manager

T. Coutu. Operations Support Manager

W. Foster, Safety Assurance Manager

J. Hampton. Vice President, Oconee Site

G. Hamrick, Manager, Chemistry

D. Hubbard, Maintenance Superintendent

C. Little, Electrical Systems/Equipment Manager

J. Smith, Regulatory Compliance

J. Twiggs, Manager. Radiation Protection

NRC

D. LaBarge. Project Manager

Enclosure 2

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Inspection Procedures Used

IP 55050:

Nuclear Welding

IP 71750:

Plant Support Activities

IP 71707:

Plant Operations

IP 61726:

Surveillance Observations

IP 62707:

Maintenance Observations

IP 37551:

Onsite Engineering

IP 92901:

Followup - Plant Operations

IP 92902:

Followup - Maintenance

IP 92903:

Followup - Engineering

IP 92700:

Onsite LER Followup

IP 73753:

Inservice Inspection

IP 84750:

Radioactive Waste Treatment, Effluent Environmental Monitoring

IP 86750:

Solid Radioactive Waste Management Transportation of Radioactive

Materi als

IP 71001:

Licensed Operator Requalification Program Evaluation

IP 71714:

Cold Weather Preparations

IP 62703:

Maintenance Observations

IP 40500:

Effectiveness of Identification and Resolving Problems

TI 2515/133:Implementation of Revised 49 CFR Parts 100-177 AND 10 CFR Part 71

  • EEnclosure

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31

Items Opened, Closed, and Discussed

Opened

50-269,270/96-16-01

VIO

Maintenance Failed To Initiate A PIP

(Section M4.1)

50-296,270,287/96-16-02

VIO

LDST Calibration Procedure In Error

(Section E8.1)

50-269,270,287/96-16-03

NCV

Failure to Provide Adequate Procedural

Guidance in the TSC Exiting a NOUE

(Section P3.1)

50-269,287/96-16-04

NCV

Failure to Maintain Equipment in

Accordance with Plant Drawings (Section

E1.2)

50-270.287/96-16-05

EEI

Failure to Properly Install MSSV Spindle

Nut Cotter Pins (Section M4.2)

50-287/96-16-06

IFI

ICS Malfunction Training Results (Section

05.1)

Closed

50-270/96-12-04

URI

Pressurizer Safety Valve 2RC-67

Operability (Section 08.1)

50-270/96-12-03

URI

Delay In LER Submittal (Section 08.2)

50-270/96-03

LER

Pressurizer Relief Valve Technically

Inoperable (Section 08.3)

50-269,270,287/96-12-02

URI

Letdown Storage Tank Pressure-Level Curves

(Section E8.1)

50-269,270.287/96-12-01

URI

MSSV Cotter Pin Inspection (Section M8.1)

Discussed

50-269/96-04-04

URI

Root Cause Assessments of Failures to

Valves IMS-77 and 1LPSW-254 (Section M8.2)

Enclosure 2

32

List of Acronyms

ABVS

Auxilary Building Ventilation System

ANI

American Nuclear Insurance

ANSI

American Nuclear Society Institute

ASME

American Society of Mechanical Engineers

BWST

Borated Water Storage lank

CFR

Code of Federal Regulations

CC

Component Cooling

CCW

Condenser Circulating Water

CoC

Certificates of Compliance

CR

Control Room

CRDM

Control Rod Drive Mechanism

DOT

Department of Transportation

DPC

Duke Power Company

EAL

Emergency Action List

ECCS

Emergency Core Cooling System

EEI

Apparent Violation

EFW

Emergency Feedwater

EOC

End Of Cycle

EOF

Emergency Operating Facility

EPRI

Electric Power Research Institute

EWST

Emergency Water Storage Tank

FWDS

Field Weld Data Sheet

FSAR

Final Safety Analysis Report

GPM

Gallons Per Minute

HAZMAT

Hazardous Material

H/L

Hot Leg

HP

Health Physics

HPI

High Pressure Injection

ICS

Integrated Control System

I&E

Instrument & Electrical

IR

Inspection Report

ISI

Inservice Inspection

KHU

Keowee Hydro Unit

LDST

Letdown Storage Tank

LER

Licensee Event Report

LCO

Limiting Condition for Operation

LOCA

Loss of Coolant Accident

LPI

Low Pressure Injection

LPSW

Low Pressure Service Water

MFP

Main Feedwater Pump

MRPC

Motorized Pancake Coil

MSOP

Main Shaft Oil Pump

MSSV

Main Steam Safety Valve

MP

Maintenance Procedure

MVA

Mega Volts-Amps

MW

Megawatts

NCV

Non-Cited Violation

  • NEnclosure

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33

0

NDE

Non-Destructive Examination

NLO

Non-Licensed Operator

NOUE

Notice Of Unusua] Event

NRC

Nuclear Regulatory Commission

NSM

Nuclear Station Modification

NSD

Nuclear System Directive

ODCM

Offsite Dose Calculation Manual

ONS

Oconee Nuclear Station

OTSG

Once Through Steam Generator

PRVS

Penetration Room Ventilation System

PSIG

Pounds Per Square Inch Gauge

PSV

Pressurizer Safety Valve

pH

Conductivity

PIP

Problem Investigation Process

PM

Preventive Maintenance

PRVS

Penetration Room Ventilation System

PWR

Pressurized Water Reactor

PWSCC

Primary Water Stress Corrosion Cracking

QA

Quality Assurance

QC

Quality Control

RBV

Reactor Building Ventilation

RCS

Reactor Coolant System

RFO

Refueling Outage

RIA

Radiation Instrument Area

RP&C

Radiological Protection & Chemistry

RPS

Reactor Protection System

RTD

Resistance Temperature Detector

TS

Technical Specification

TSC

Technical Support Center

UFSAR

Updated Final Safety Analysis Report

URI

Unresolved Item

WO

Work Order

WR

Work Request

  • yEnclosure

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