ML14181A973

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Insp Rept 50-261/97-12 on 971012-1122.Violations Noted. Major Areas Inspected:Operations,Maintenance,Engineering & Plant Support
ML14181A973
Person / Time
Site: Robinson 
Issue date: 12/22/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14181A971 List:
References
50-261-97-12, NUDOCS 9801210300
Download: ML14181A973 (34)


See also: IR 05000261/1997012

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos:

50-261

License Nos:

DPR-23

Report No:

50-261/97-12

Licensee:

Carolina Power & Light (CP&L)

Facility:

H. B. Robinson Unit 2

Location:

3581 West Entrance Road

Hartsville, SC 29550

Dates:

October 12 - November 22, 1997

Inspectors:

B. Desai, Senior Resident Inspector

J. Zeiler, Resident Inspector

E. Girard, Region II Inspector (Sections

E1.1, E1.2, and E7.1)

H. Whitener. Region II Inspector (Section M1.2)

Accompanying Personnel: T. Scarborough, Nuclear Reactor Regulation

Approved by:

M. Shymlock, Chief, Projects Branch 4

Division of Reactor Projects

9801210300 971222

Enclosure 2

PDR

ADOCK 05000261

G

PDR

EXECUTIVE SUMMARY

H. B. Robinson Power Plant, Unit 2

NRC Inspection Report 50-261/97-12

This integrated inspection included aspects of licensee operations,

maintenance, engineering, and plant support. The report covers a six-week

period of resident inspection; in addition, it includes the results of

inspections by two Region II based reactor safety inspectors.

Operations

The conduct of operations was professional and safety-conscious.

(Section 01.1).

Overall, operator response to the failure of a condensate pump shaft and

subsequent automatic reactor trip was appropriate. Plant shutdown and

startup activities were satisfactorily conducted. Ineffective

corrective actions from a similar condensate pump shaft failure that

occurred in 1991 resulted in the subsequent failure on November 16, 1997

(Section 01.2).

Two Non-Cited Violations (NCVs) were identified involving operator

failure to follow procedures while implementing Technical Specification

(TS) surveillance requirements. While individually, each of these items

had low safety consequence, they indicated weaknesses in operator log

keeping accuracy and operator attention to detail (Section 01.3).

Overall, licensee implementation of cold weather protection activities

was satisfactory and the system engineer was familiar with plant cold

weather protection equipment. Additionally, a Nuclear Assessment

Section (NAS) audit of the plant cold weather protection activities was

thorough, and condition reports were appropriately initiated to address

several deficiencies that were identified by the NAS audit (Section

02.1).

The licensee's implementation and transition to the Improved Technical

Specifications was good (Section 06.1).

The onsite review functions of the Plant Nuclear Safety Committee (PNSC)

were conducted in accordance with TS. The PNSC meetings were well

coordinated and meeting topics were thoroughly discussed and evaluated.

NAS continued to provide strong oversight of licensee activities. A NAS

assessment of the Robinson Motor-Operated Valve program was thorough and

resulted in important findings (Section 07.1 and E7.1).

The failure to properly implement Regulatory Guide commitments as

described in the Updated Final Safety Analysis Report (UFSAR) associated

with the Loose Parts Monitoring Program was considered similar to

deficiencies and inconsistencies in the UFSAR and other licensing

documents previously identified during the NRC's Architectural

Engineering (A/E) Team Inspection (Section 08.1).

2

Maintenance

In general, routine maintenance activities were performed satisfactorily

(Section M1.1).

Emergency diesel generator (EDG) maintenance management indicated

advanced planning and careful attention to detail.

EDG post-maintenance

testing was performed in a thorough and professional manner. The

licensee thoroughly researched potential sources of vibration

experienced on the "B" EDG and planned further evaluations during an

upcoming planned diesel maintenance outage. The "B" EDG vibration data

exceeded the in-service limit but was well below the vendor recommended

shutdown limit (Section M1.2).

Engineering

An Inspector Followup Item (IFI) was opened related to an event

involving the lifting of a relief valve on the Safety Injection (SI)

discharge piping during an Inservice (ISI) test. The licensee's

evaluation of the condition concluded that it did not adversely impact

the SI system nor did it impact accident dose. The inspector concluded

that the condition did not significantly compromise safety; however,

several issues are still under review (Section E1.1).

The licensee had not met its original commitment date for correcting

adverse findings regarding its implementation of Generic Letter (GL) 89-10 identified during NRC Inspection 50-261/96-12. Progress toward

correcting the findings by the new date proposed by the licensee was

generally satisfactory. Some concerns were identified. These concerns

and the outstanding findings from NRC Inspection 50-261/96-12 will be

re-examined in a future inspection which will assess the licensee's

completion of GL 89-10 implementation (Section E1.2).

A Violation was identified for the failure to adequately control post

modification testing related to ESR 9500783. The post-modification

testing failed to confirm that the cooling performance of the

Containment Air Recirculation Cooling system was not adversely impacted,

and that the system was capable of meeting its intended safety function

as described in Section 9.4.3.1 of the licensee's UFSAR (Section E8.3).

Plant Support

The inspectors concluded that radiation control and security practices

were proper (Section R1.1 and S1.1).

Report Details

Summary of Plant Status

Robinson Unit 2 began the inspection period operating at full power. The unit

tripped from 100 percent power on November 16, 1997, due to mechanical failure

of the "B" Condensate Pump shaft. The condensate pump was repaired and the

unit went critical on November 19. Synchronization to the grid occurred on

November 20. The unit reached essentially full power operation the next day

and continued at essentially full power for the remainder of the inspection

period. Up until the day of the trip, the unit had operated at power for 390

continuous days.

I. Operations

01

Conduct of Operations

01.1 General Comments (71707)

The inspectors conducted frequent control room tours to verify proper

staffing, operator attentiveness and communications, and adherence to

approved procedures. The inspectors attended daily operation turnovers,

management reviews, and plan-of-the-day meetings to maintain awareness

of overall plant operations. Operator logs were reviewed to verify

operational safety and compliance with Technical Specifications (TSs).

Instrumentation, computer indications, and safety system lineups were

periodically reviewed from the Control Room to assess operability.

Frequent plant tours were conducted to observe equipment status and

housekeeping. Condition Reports (CRs) were routinely reviewed to assure

that potential safety concerns and equipment problems were reported and

resolved.

In general, the conduct of operations was professional and safety

conscious; specific events and noteworthy observations are detailed in

the sections below.

01.2 Reactor Trip and Subsequent Unit Startup

a. Inspection Scope (71707 and 93702)

On November 16, 1997, at approximately 1:33 a.m., Robinson Unit 2

experienced an automatic reactor trip. The unit was operating at full

power prior to the transient. The Senior Resident Inspector was

notified and responded to the site. A 10 CFR 50.72 (b)(2)(ii)

notification was appropriately made to the NRC. The inspector reviewed

the circumstances associated with the reactor trip, as well as the

subsequent plant startup activities.

b. Observations and Findings

Robinson Unit 2 experienced an automatic reactor trip due to low (26

percent) Steam Generator (S/G) level coincident with Steam

Flow/Feedwater flow mismatch. All control rods inserted into the core

and electrical power transferred to the startup transformer without any

2

problems. The transient was initiated when the "B" Condensate Pumps'

stub shaft sheared. The condensate pumps are deep draft centrifugal

pumps and have a long shaft connecting the motor to the pump. The stub

shaft is a coupling that connects the long shaft to the pump shaft.

S/G levels trended down due to the loss of the condensate pump. The

control room entered Abnormal Operating Procedure (AOP) 010, Main

Feedwater/ Condensate Malfunction, upon noticing decreasing S/G levels.

The "B" Condensate Pump motor continued to run and the stub shaft shear

was initially unknown to the operators since there is no motor ammeter

or individual condensate flow/pressure indication in the control room.

Due to the ongoing transient, the operator initiated a Turbine runback.

However, S/G level continued to decrease and the runback caused a

Reactor Coolant System (RCS) Temperature (T)-average/T-reference

mismatch. This mismatch caused the condenser dump valves to open,

causing steam flow to be greater than feedwater flow, resulting in a

reactor trip.

Plant post trip response was normal with some exceptions. Source Range

(SR) Nuclear Instruments (NI) 31 and NI 32 did not automatically

energize at permissive P-6. Consequently, NIs 31 and 32 had to be

manually energized. Additionally, Intermediate Range (IR) instruments

NI 35 was noted to have failed and IR NI 36 was noted to be slightly

under compensated. P-6 is actuated when both IR NIs 35 and 36 reach 1E

10 amperes. With the failure of NI 35, P-6 was not received causing

failure of NIs 31 and 32 to automatically energize. The problem with NI

36 was later attributed to a loose power supply cable connection, and NI

36 was returned to operable status following corrective maintenance.

The problem with NI 35 was identified to be a failed detector. The

detector was replaced and NI 35 was also returned to service prior to

reactor startup.

Initially, the control room was not aware of the stub shaft failure.

However, during the investigation after the reactor trip, an abnormal

noise was heard at the pump. The motor was noted to be running;

however, the local ammeter reading as well as pump discharge pressure

were noted to be abnormally low, indicative of a shaft failure. The

condensate pump was subsequently disassembled and the stub shaft failure

was confirmed. The licensee replaced the "B" pump with a spare pump and

installed a new designed stub shaft.

The inspector examined the failed stub shaft and reviewed the licensee's

preliminary investigation into the cause of the shaft failure. The stub

shaft had sheared in the vicinity of the split ring grove at the top

portion of the keyway grove. This failure was considered similar to the

one that occurred in September 1991 on the same pump. The 1991 failure

was attributed to a faulty design of the stub shaft keyway area. The

keyway was machined into the split ring grove area and contained sharp

corners that created stress riser locations. In 1991, following

discussions with the pump manufacturer, it was discovered that a new

stub shaft keyway design existed that eliminated the stress riser

problem. The licensee ordered three stub shafts with the new keyway

design with the intent to replace each of the stub shafts on the three

3

condensate pumps. In the interim, an old design stub shaft (with slight

modifications to the keyway area) was installed in the "B" Condensate

Pump following the initial failure.

In December 1991, a refurbished pump was installed in the "B" Condensate

Pump, however, a stub shaft of the new design was not installed, and

instead, the old stub shaft was cleaned and re-installed. The licensee

attributed the failure to replace the stub shaft with the new design,

due to poor wording on the work ticket and lack of effective engineering

coordination. During the September 1996 refueling outage, the "B"

Condensate Pump was again removed and replaced with a refurbished pump

as part of preventative maintenance; however, again, the old stub shaft

was reused. The inspector determined that ineffective corrective

actions from the previous stub shaft failure incident in 1991

contributed to the subsequent stub shaft failure on November 16, 1997.

Following completion of a post trip review, which addressed the cause of

the trip and corrective actions, the licensee initiated plant startup on

November 19, 1997 in accordance with General Procedure (GP)-003, Normal

Plant Startup From Hot Shutdown to Critical.

The plant was placed on

line on November 20, 1997.

The inspector reviewed plant logs and post trip report, discussed the

event with key licensee personnel, and walked down plant equipment,

including maintenance activities associated with the condensate pump

replacement. The inspector also monitored plant startup activities.

c. Conclusions

The inspector concluded that overall, operator response to the transient

was appropriate. Plant shutdown and startup activities were

satisfactorily conducted. With the regard to the condensate pump, the

inspector determined that ineffective corrective actions from a similar

stub shaft failure that occurred in 1991 contributed to resulted the

subsequent failure and reactor trip on November 16, 1997.

01.3 Failure to Follow Procedures Implementing TS Surveillance Requirements

a. Inspection Scope (71707)

The inspector reviewed the circumstances surrounding two examples where

operations personnel failed to follow procedures related to implementing

TS surveillance requirements during the startup from the November 16,

1997, reactor trip.

b. Observations and Findings

1. Failure to Log TS Surveillance for Inoperable Control Rod Insertion

Limit Monitor

On November 18, the operators observed that the control rod insertion

limit monitor (RILM) recorder, TR-409, was not printing all of the rod

4

insertion limits. As a result of this condition, the RILM was declared

out-of-service. On November 19, 1997, after entering Mode 2, operations

recognized the need to perform TS Surveillance Requirement (SR) 3.1.6.2,

which is required when the RILM is considered inoperable. This

surveillance required each control bank insertion to be verified within

its limit as specified in the Core Operating Limits Report (COLR) every

four hours.

On November 20, 1997, during a review of the Reactor Operator (RO)

narrative log, the inspector noted that the first four hour surveillance

had been logged as complete at 7:35 p.m. on November 19. The next log

entry documenting the surveillance completion was at 3:32 a.m., on

November 20. The inspector noted that there was no log entry indicating

that the surveillance had been performed as required at 11:30 p.m. on

November 19. The licensee initiated CR 97-02328 to address the

discrepancy.

The licensee's preliminary investigation indicated that the operators

had recalled performing the four hour surveillance at 11:30 p.m.

However, the operators failed to properly log completion of the

surveillance in their log. The inspector discussed the impact of the

original problem with the RILM recorder with the system engineer and

agreed with the licensee's conclusion that this problem would not have

impacted the RILM's alarm function. Therefore, although the monitor had

been declared inoperable, it would have still been capable of alerting

the operators to an insertion limit problem during this time period.

The inspector reviewed Operations Surveillance Test (OST)-020, Shiftly

Surveillances, Revision 2, which provides instructions for performing TS

required shiftly surveillances. OST-020 requires that when the RILM is

inoperable, the control rod bank insertion limit be verified within the

limits specified in the COLR once within four hours and every four hour

thereafter, and the performance of this activity entered into the RO's

narrative log. The inspector determined that the operators failed to

follow OST-020. Prior to this incident, the inspector's had noted an

increase in errors and inconsistencies in operator logs which indicated

a need for improvement in attention to detail and log keeping accuracy.

The inspector determined that increased management attention to the

quality of log keeping was warranted.

TS 5.4, Procedures, requires in part that written procedures be

established, and maintained covering the activities recommended in

Appendix A of Regulatory Guide 1.33, Revision 2, dated February 1978,

including procedures for conducting surveillances listed in the TS. The

inspector determined that the failure to follow OST-020 was a violation

of TS 5.4. This failure constitutes a violation of minor significance

and is being treated as a Non-Cited Violation (NCV), consistent with

Section IV of the NRC Enforcement Policy. This issue is documented as

NCV 50-261/97-12-01:

Failure to Log TS Surveillance Completion in

Accordance with OST-020.

5

2. Missed TS Surveillance of Reactor Coolant Dose Equivalent Iodine-131

On November 20, 1997, at 5:38 p.m., the RO noticed that reactor coolant

dose equivalent Iodine (I)-131 specific activity had not been verified

as required by TS SR 3.4.16.2. SR 3.4.16.2 requires that within six

hours after a thermal power change of greater than 15 percent power in a

one hour period, reactor coolant dose equivalent 1-131 be verified less

than or equal to 1 microcurie per gram. Reactor power was increased

greater than 15 percent between 10:00 a.m. and 11:00 a.m. on

November 20, requiring SR 3.4.16.2 to be completed by 5:00 p.m. Upon

identifying the missed surveillance, immediate operator actions were

implemented to request Environmental and Radiation Control (E&RC)

personnel to sample the Reactor Coolant System (RCS).

The sample was

taken at 6:05 p.m. and the results obtained at 8:18 p.m. The results

indicated that the reactor coolant dose equivalent 1-131 specific

activity was much less than the TS limits.

The inspector reviewed GP-005, Power Operation, Revision 53, which

provides instructions to permit normal plant startup from Mode 2 to

Mode 1 at 100 percent power. Section 5.4.33 of GP-005 requires the

operators to contact E&RC personnel following any load change greater

than or equal to 15 percent power in order for dose equivalent 1-131 to

be verified with six hours. The inspector determined that operations

personnel failed to follow GP-005 resulting in SR 3.4.16.2 not being

performed within the allowed timeframe.

The licensee initiated CR 97-02342 to investigate the missed

surveillance requirement. The licensee determined that the surveillance

was missed due to lack of operator attention to detail and inadequate

supervisory oversight during periods of high control room activities.

The inspector noted that one of the significant contributing factors

identified was a weakness in GP-005's control of the activity. The step

for performing the surveillance was placed at the point where reactor

power would have just reached 15 percent power, as opposed to being in a

continuous monitoring section of the procedure, such as the precautions

and limitations. Once the step was signed off at 15 percent power,

there was no further mention of the surveillance requirement during

subsequent power ascension activities. The licensee planned to revise

GP-005 to ensure that the surveillance requirement was reiterated in the

precautions and limitations section of the procedure.

TS 5.4, Procedures, requires in part that written procedures be

established, and maintained covering the activities recommended in

Appendix A of Regulatory Guide 1.33, Revision 2, dated February 1978,

including procedures for conducting surveillances listed in the TS. The

inspector determined that the failure to follow GP-005 was a violation

of TS 5.4. This non-repetitive, licensee-identified and corrected

violation is being treated as a NCV, consistent with Section VII.B.1 of

the NRC Enforcement Policy. This issue is documented as NCV 50-261/

97-12-02:

Failure to Verify Dose Equivalent 1-131 in Accordance with

GP-005.

6

c. Conclusions

Two NCVs were identified involving operator failure to follow procedures

for implementing TS surveillance requirements. While individually, each

of these items had low safety consequence, they indicated weaknesses in

operator log keeping accuracy and operator attention to detail,

warranting licensee attention.

02

Operational Status of Facilities and Equipment

02.1 Cold Weather Preparations

a. Inspection Scope (71707)(71714)

The inspector assessed licensee preparations and contingencies for cold

weather conditions, as well as performed a walkdown of the related

freeze protection panels and temporary cold weather protection measures.

b. Observations and Findings

The inspector reviewed Administrative Procedure (AP)-008, Cold Weather

Preparations, Operating Procedure (OP)-925, Cold Weather Operation, and

Electrical Distribution Procedure (EDP)-009, Freeze Protection Panels,

to assess licensee preparations and contingencies associates with cold

weather, and existing CRs associated with cold weather protection

problems. The inspector also performed a walkdown with the system

engineer of freeze protection panels and other selected components,

including: the service water intake area, deepwell pumps, installed

temporary heaters and enclosures, and temperature sensing instruments

that control the thermostats associated with the freeze protection

circuits. Additionally, the inspector reviewed existing CRs related to

cold weather preparations and a program audit that was performed by the

Nuclear Assessment Section (NAS).

c. Conclusions

The inspector concluded that the system engineer was familiar with the

system, the NAS audit was thorough, and overall licensee implementation

of the cold weather protection measures was satisfactory. The licensee

appropriately generated condition reports to address several

deficiencies that were identified by the NAS audit.

06

Operations Organization and Administration

06.1 Improved Technical Specification Implementation

a. Inspection Scope (71707)

The inspector reviewed licensee activities associated with the

implementation of Improved Technical Specifications (ITS).

The ITS was

implemented at Robinson on November 13, 1997, following issuance of

License Amendment No. 176.

7

b. Observations and Findings

Concurrent with the ITS, the licensee also implemented the ITS Bases, as

well as the Technical Requirements Manual(TRM), through Plant Program

Procedure (PLP)-100. PLP-100 incorporated requirements from the

previous Technical Specifications that were no longer part of ITS. The

inspector observed licensee utilization of the ITS during evolving plant

issues, including the recent reactor trip and subsequent startup

activities. The inspector observed that, overall, the licensee was

familiar with the requirements of ITS, and as necessary, sought

appropriate guidance, in view of the change in the overall format from

the previous TS. The licensee also stationed, in the control room, an

individual who had participated in the development of ITS. This allowed

the operating staff to ask questions as they related to the ITS to this

individual, as necessary. Additionally, the licensee canceled all

existing TS interpretations.

c. Conclusions

The inspector concluded that licensee implementation, as well as

transition to ITS, was good. The licensee did a good job of

implementing the new ITS surveillance requirements following a reactor

trip only three days after putting them in place.

07

Quality Assurance In

Operations

07.1 Plant Nuclear Safety Committee and Nuclear Assessment Section Oversight

a. Inspection Scope (40500)

The inspector evaluated certain activities of the Plant Nuclear Safety

Committee (PNSC) and NAS to determine whether the onsite review

functions were conducted in accordance with TS and other regulatory

requirements.

b. Observations and Findings

The inspector periodically attended PNSC meetings during the report

period. The presentations were thorough and the presenters readily

responded to all questions. The committee members asked probing

questions and were well prepared. The committee members displayed a

good understanding of the issues and their potential risks.

Further,

the inspector reviewed NAS audits and concluded that they were

appropriately focused to identify and enhance safety.

c. Conclusions

The inspector concluded that the onsite review functions of the PNSC

were conducted in accordance with TSs. The PNSC meetings attended by

the inspector were well coordinated and meetings topics were thoroughly

discussed and evaluated. NAS continued to provide strong oversight of

licensee activities.

8

08

Miscellaneous Operations Issues (92901)

08.1 (Closed) Unresolved Item (URI) 50-261/97-10-01, Complete Review of LPMS

Testing and Maintenance Activities:

This URI involved the completion of

a review of the licensee's Loose Parts Monitoring System (LPMS) program.

The inspector previously identified the potential that the licensee's

LPMS program was not implemented in accordance with their commitments

associated with Regulatory Guide (RG) 1.133, Loose Parts Detection

Program for the Primary System of Light Water Cooled Reactors,

Revision 1. Specifically, Section C.3 of RG 1.133 recommended the

performance of 31-day channel functional tests and 92-day background

noise and channel false signal checks. In addition, the inspector noted

from review of the LPMS vendor manual that the backup battery, which

provides display and memory power, was recommended to be replaced every

six months; however, the licensee had implemented an 18-month

replacement frequency. At the end of the previous inspection period,

the licensee had not demonstrated that these tests were being performed

or had justified the impact of the increased battery replacement

schedule.

On November 20, 1997, the licensee initiated CR 97-2331 to address the

inspector's concerns regarding the testing discrepancies. In addition,

the licensee initiated an engineering self-assessment of the LPMS

testing program. The results of the self-assessment confirmed that the

above mentioned testing was not being performed as recommended by RG

1.133. Licensee corrective actions included plans to revise LPMS

procedures to incorporate the periodic channel functional testing and

background noise/false signal checks. At the end of this report period,

the licensee was still evaluating whether the RG recommended test

frequencies were appropriate. Following resolution of the test

frequencies, the licensee planned to update UFSAR Section 1.8 to reflect

any difference in their position from the recommendations in RG 1.133.

With regards to the backup battery replacement frequency, the licensee

contacted the LPMS vendor supplier and determined that the 18-month

frequency was adequate to ensure that the equipment power requirements

would not be compromised. In addition, the vendor indicated that the

system was designed to alarm on low backup battery power, which would

alert the licensee to a low battery power condition. The inspector

determined that the licensee had adequately addressed the inspector's

concerns associated with the LPMS testing and maintenance.

Section 1.8 of the licensee's Updated Final Safety Analysis Report

(UFSAR) indicated that Robinson was in full compliance with RG 1.133

with the exception of two items. These two exceptions were unrelated to

the recommended testing associated with the LPMS. The inspector

determined that the licensee had not fully implemented LPMS testing in

accordance with their UFSAR commitments. Furthermore, this problem

raised questions regarding the adequacy in the implementation of other

UFSAR commitments related to RGs. During the NRC Architectural

Engineering (A/E) Team Inspection conducted in May 1997, similar

inconsistencies and deficiencies were identified in the UFSAR. In the

licensee's letter dated November 3, 1997, replying to the results of the

9

A/E Team Inspection, the licensee committed to review all of their RG

positions included in the UFSAR to ensure proper implementation. The

inspector determined that, in view of the weaknesses already identified

in the licensee's RG implementation, and proposed licensee corrective

actions to address this problem, no further enforcement action was

warranted for this issue. The adequacy of the licensee's corrective

actions will be reviewed during the closeout review of the A/E Team

Inspection findings. This URI is closed.

II.

Maintenance

M1

Conduct of Maintenance

M1.1 General Comments

a. Inspection Scope (61726 and 62707)

The inspector reviewed/observed all or portions of the following

maintenance related work requests/job orders (WRs/JOs) and/or

surveillances and reviewed the associated documentation:

WR/JO 97-AEYU1

Perform Vertical Drive Inspection on "B"

Emergency Diesel Generator (EDG)

WR/JO AAPV-002

Inspections and Overhaul Maintenance on "B" EDG

WR/JO AAKC-007

Inspections and Overhaul Maintenance on "A" EDG

OST-409-2

EDG "B" Fast Speed Start

b. Observations and Findings

The inspector observed that these activities were performed by personnel

who were experienced and knowledgeable of their assigned tasks.

Procedures were present at the work location and being followed.

Procedures provided sufficient detail and guidance for the intended

activities. Activities were properly authorized and coordinated with

operations prior to starting. Test and maintenance equipment in use was

calibrated, procedure prerequisites were met, and system restoration was

completed. The inspector frequently observed supervisors and system

engineers monitoring the "A" and "B" EDG maintenance activities, and

good support was noted from the EDG vendor.

c. Conclusions

The inspector concluded that routine and corrective maintenance

activities, as well as surveillances, were performed satisfactorily.

M1.2 EDG Vibration Investigation and 18 Month Inspection

a. Inspection Scope (62700, 62707 and 92902)

The inspector reviewed licensee activities to monitor, trend and

investigate a diesel generator vibration problem. Additionally, the

inspectors reviewed the licensee's methods for control of a complex

10

project, 18 month EDG surveillance, and observed portions of an

overspeed trip test.

b. Observations and Finding

The licensee removed the "B"

EDG from service on October 20, 1997 to

investigate vibrations and to conduct an 18 month surveillance. The

Robinson EDGs are Fairbanks Morse opposed piston engines. The method

used by the licensee to control the EDG maintenance activities was to

develop a detailed maintenance schedule. One hundred and seven specific

tasks were identified and scheduled by group, day, and hour. Each task

was implemented by either the PM route or a work package. Completion of

the tasks was tracked by the automatic maintenance management system and

work status was reviewed daily at management and plan of the day

meetings. The inspector considered that the project was well planned

and careful attention to detail was noted.

The inspector discussed the condition of EDG vibrations with licensee

personnel. Actions taken during this diesel testing period included

taking data to develop actions for the planned EDG outage in the

January-February 1998 time frame to specifically address the vibration

problem. Additionally, licensee work activities included checking the

upper and lower thrust bearings for free play, checking the total run

out on the engine to generator coupling for unbalanced mass, and

checking the bolt torque and delivery stroke of the fuel injection pumps

to ensure that no unbalanced firing was occurring. In addition, four

injection pumps were replaced.

From the data taken, the licensee determined that the vibration appeared

to be load rather than speed related. Several areas were identified as

potential sources of vibration to be examined at the planned EDG outage

in early 1998. These included the vertical drive spring pack, torsional

dampers on the crank shaft, alignment of engine to generator coupling

and the generator outboard bearing.

The inspector observed portions of the overspeed trip test performed as

a part of OP-604, Diesel Generators "A"

and "B," Revision 40, during

post maintenance diesel start-up. The pre-job briefing was adequate and

the crew was knowledgeable and adequate resources were available.

Maintenance, engineering, and operator responsibilities were reviewed.

The engine was inspected for leaks or problems as the speed was

increased. The licensee stated that data taken during the post

maintenance run indicated that there was a slight improvement in the

vibration level.

The inspector reviewed the vibration trended data from October 1996 to

October 1997. The data are taken monthly at thirteen locations. There

was an increase since June 1997 in vibration levels at several locations

which exceeded the in-service limit. However, these data were well

below the vendors recommended shutdown limit. Unless there are

significant changes in the increase of vibrations, the shutdown limits

are not expected to be exceeded before the planned diesel maintenance

outage.

c. Conclusions

EDG maintenance management indicated advanced planning and careful

attention to detail. The licensee thoroughly researched potential

sources of vibration to be evaluated at the January-February 1998

planned diesel maintenance outage. EDG post-maintenance testing was

performed in a thorough and professional manner. The "B" EDG vibration

data exceeded the in-service limit but was well below the vendor

recommended shutdown limit.

III. Engineering

El

Conduct of Engineering

E1.1 Pressure Testing of Safety Injection Pump Discharge Piping

a. Inspection Scope (37551)

The inspector reviewed an event where relief valve SI-857A, located on

the Safety Injection (SI) discharge piping lifted during the performance

of an Inservice Inspection (ISI) pressure test.

b. Inspection Findings

On November 12, 1997, the licensee performed Engineering Service Test

(EST) procedure, EST-078, ISI Pressure Testing of Safety Injection Pump

Discharge Piping. This ISI was performed in conjunction with Operations

Test Procedure (OST) 151-1, Safety Injection System Components Test Pump

"A". During the performance of EST-078, the SI system was placed in

service in accordance with procedure OST-151-1 and the system was

visually examined for leakage within the boundaries established by

procedure EST-078. This boundary including piping, valves, and

instrumentation taps, from the SI pump discharge up to the containment

penetration. During the performance of the ISI, a Quality Control (QC)

inspector noted a pencil size stream of water discharging from the tail

pipe of relief valve SI-857A. This leak was estimated to be

approximately one gallon per minute (gpm) and it was terminated when the

piping was depressurized following completion of the EST.

Relief valve SI-857A is physically located in the Boron Injection Tank

(BIT) room in the auxiliary building. The SI cold leg discharge piping

downstream of the BIT includes a single line with relief valve SI-857A.

Then the line splits into two, and includes two normally closed MOVs

SI-870A and SI-870B. The line downstream of SI-870A and SI-870B combine

and then splits into three lines, which include normally open valves

868A, 868B, and 868C. The three SI cold leg injection lines then enter

containment, and include a relief valve SI-857B, which reliefs to the

Pressurizer Relief Tank (PRT).

Each of the three SI injection lines

then have two check valves in series (873A and 873D, 873B and 873E, and

12

873C and 873F).

The three SI lines then tie into the three

Accumulator/Residual Heat Removal (RHR) injection lines. These three

lines, each have a check valve (875A, 875B. and 875C), prior to the

three lines tying to the RCS cold leg loops. The SI piping downstream

of valves 868A, 868B, and 868C is rated as class 2500 (capable of

withstanding full RCS pressure) and the piping upstream of valves 868A,

868B, and 868C is rated as class 1501 (capable of withstanding 1750 psig

at 300 degrees F and 1900 psig at 150 degrees F).

Relief valves SI-857A

and 857B are set to relieve at 1767 +/- 51 psi.

During the performance of EST-078, the A SI pump was run discharging at

a pressure of approximately 1500 psig. When valves SI-870A and SI-870B

were opened to allow pressurization of downstream SI piping, relief

valve SI-857A lifted. The licensee considered that the RCS check valves

868A, 868B, and 868C leaked into the pipe upstream of valves 870A and

870B. With the relief setpoint for SI-857A slightly lower then SI-857B

(within the allowed tolerance of +/- 51 psi), relief valve SI-857A

lifted to relieve pressure buildup.

Engineering Service Request (ESR) 9700594 was initiated to address

potential adverse issues related to this problem. First, the ESR

assessed the implications of relief valve (857A) lifting during an

accident and the subsequent radiological release. Specifically, during

a small break Loss of Coolant Accident (LOCA), where valves SI-870A and

SI-870B would open on an SI signal and the SI pump would start; however,

due to high RCS pressure, SI discharge pressure would be below RCS

pressure. During this time, relief valve 857A would be subject to

similar pressure conditions from backleakage through the check valves,

causing the relief valve to lift. The licensee concluded that the relief

valve leakage would not present a significant radiological consequence,

and under worst case source term assumptions, was still bounded by

existing analysis.

The licensee also evaluated the potential degradation of SI flow in view

of the potential for relief valves 857A and 857B lifting following a

small break LOCA. Further, the leakage from 857A would be outside

containment, and therefore unavailable during recirculation flow. The

relief valves are designed with a 3/4 inch inlet and a 1 inch outlet.

An internal nozzle further restricts the flow to that of a 1/4 inch

diameter pipe. The licensee concluded that existing calculation RNP

M/MECH-1556, Attachment G, demonstrated acceptable system performance

with losses from an open SI test line, and it effectively bounded the

above postulated condition. The inspector had not reviewed the

calculation as of the end of this report period.

The licensee evaluated the acceptability of class 1501 piping upstream

of normally open valves 868A, 868B, and 868C. The licensee concluded

that the lift setpoint of 1750 psig to 1900 psig for a temperature range

of 300 degrees to 150 degrees F adequately afforded the design limits of

the piping from being exceeded. The inspector had not completed the

0s

review associated with this aspect of the evaluation.

13

Additionally, the inspector is reviewing several additional related

issues. These include: the differential pressure testing and

requirements associated with valves SI-870A and SI-870B, the

acceptability of a single isolation valve to afford protection against a

potential leak outside containment, and the check valve backleakage test

methodology and acceptance criteria. Pending completion of the reviews

associated with this problem, the item is identified as Inspector

Followup Item (IFI) 50-261/97-12-03: Review Safety Injection Discharge

Piping Configuration.

The licensee has placed caution tags on the three SI pumps' control

switches in the control room. Periodic testing of SI-870A and SI-870B

requires them to be opened. This presents the potential for lifting

relief valve 857A. The caution tags allows the operator to be cognizant

of this potential and to place an observer in the BIT room or to take

other appropriate actions, including entry in appropriate TS action

statement, as necessary. The licensee is also considering additional

actions through the resolution of the CR system.

c. Conclusions

The inspector opened an IFI related to an event involving lifting of a

relief valve on the SI discharge piping during an ISI test. Licensee

evaluated the condition and concluded that it did not adversely impact

the SI system nor did it impact accident dose. The inspector concluded

that the condition did not significantly compromise safety; however,

several issues still are under review.

E1.2 Implementation of Generic Letter (GL) 89-10,"Safety-Related Motor

Operated Valve Testing and Surveillance"

a. Inspection Scope (Temporary Instruction 2515/109)

The licensee's implementation of GL 89-10, was previously reviewed and

determined inadequate during a previous inspection as documented in NRC

Inspection Report 50-261/96-12. Two violations were identified (see

E8.1 and E8.2) which addressed the principal deficiencies in the

licensee's implementation of GL 89-10. The licensee responded to the

violations in letters dated January 15 and February 28, 1997, and stated

that full compliance with requirements would be achieved by

September 29, 1997. In addition, the licensee indicated that a self

assessment would be performed by that date to confirm adequate

implementation of GL 89-10 and readiness for an NRC closure inspection.

In a letter dated June 30, 1997, the licensee changed the completion

date for evaluations and calculation revisions being performed as part

of its corrective actions, but did not change the date for full

compliance with requirements. Subsequently, in a telephone call on

September 24 and a letter dated September 26, 1997, the licensee

informed the NRC that it would not be ready for the closure inspection

due to issues identified in its self-assessment. The letter stated that

Robinson would be ready for a GL 89-10 closure inspection by

February 16, 1998.

14

The current inspection assessed the procedures, calculations, and

evaluations which the licensee was revising or preparing to address the

adverse findings of Inspection 50-261/96-12 and complete implementation

of GL 89-10. It included a review of the self-assessment referred to in

the previous paragraph, which is described in E7.1. The inspection also

re-examined the licensee's implementation of a GL 89-10 recommendation

to periodically examine motor-operated valve (MOV) data for trends.

This recommendation had previously been examined and found

satisfactorily implemented during Inspection 50-261/94-06. It was re

examined to verify that it remained satisfactorily implemented and,

especially, to determine if the related records indicated any adverse

trends in MOV operability.

The inspection was conducted through reviews of documentation and

interviews with licensee personnel. The documents reviewed included:

CP&L GL 89-10 Corporate Improvement Plan, Revision 1.

CP&L Nuclear Generation Group Standard Procedure EGR-NGGC-0101,

"Electrical Calculation of Motor Output Torque for AC and DC Motor

Operated Valves (MOVs)," Revision 1.

CP&L Nuclear Generation Group Standard Procedure EGR-NGGC-0203,

"Motor-Operated Valve Performance Prediction, Actuator Settings,

and Diagnostic Test Data Reconciliation," Revision 3.

Engineering Service Request ESR-9700328, "Determination of MOV

Rate-of-Loading Factors," Revision 0, dated August 6, 1997.

Engineering Service Request ESR-9700330, "Determination of MOV

Valve Factors," Revision 0, dated August 7, 1997.

Sample MOV calculation packages.

Summary tabulations of MOV information and calculation results,

including a list of MOV "available valve factors" calculated using

formulas described in previous inspection reports.

Other licensee documents were reviewed, in part, as described in

subsequent paragraphs.

b. Observations and Findings

1. Procedures, Calculations, and Evaluations Revised/Prepared to Address

Findings From Inspection 50-261/96-12

MOV Sizing and Switch Settings

The licensee had revised Procedure EGR-NGGC-0203 to provide updated

guidance on MOV sizing and settings. Licensee personnel stated that

further revision was planned, to reflect additional information obtained

in ongoing reviews. The inspectors' review of the current procedure

(Revision 3) and found it generally satisfactory but identified various

concerns which will be evaluated further in a GL 89-10 closure

inspection for Robinson. Examples were as follows:

Section 3.34 of EGR-NGGC-0203 defined valve factor as the valve

disc-to-seat friction factor. The inspectors noted that valve

15

factor can also be influenced by guide-to-disc friction and metal

interference. The licensee personnel agreed and stated that the

definition of valve factor would be revised.

Section 9.3.3 of EGR-NGGC-0203 in Paragraph 1 provided guidance

for the determination of the minimum required actuator diagnostic

torque for butterfly valves. The inspectors noted that the

guidance did not include the consideration of potential spring

pack relaxation. Licensee personnel agreed and stated that spring

pack relaxation will be addressed.

A note in Paragraph 1 of Section 9.3.4 of EGR-NGGC-0203 stated

that, in certain applications, it may be justified to assume a

minimum available motor torque based on voltage conditions other

than design-basis conditions. The inspectors noted that the

assumption of degraded voltage different from design-basis

conditions must be carefully justified.

Section 9.4.2 of EGR-NGGC-0203 described the setting of MOV limit

switches based on handwheel and wormshaft revolutions. The

inspectors noted that a more precise method of verifying limit

switch settings (such as diagnostic trace analysis) may be needed

if the actuator is controlled by the limit switch setpoint.

Section 9.4.5 of EGR-NGGC-0203 provided guidance for the

calculation of valve stroke time. The inspectors noted that the

method in EGR-NGGC-0203 might not provide accurate predictions of

valve stroke time for dc-powered MOVs. Licensee personnel

understood the concern, but stated that there are currently no dc

powered MOVs at Robinson.

Section 9.5.2 of EGR-NGGC-0203 provided guidance for the

evaluation of motor stall failures for MOVs. The inspectors noted

that the guidance did not discuss evaluation of the effect of the

stall on motor performance or key/yoke structural integrity.

Licensee personnel agreed, and stated that the guidance would be

clarified.

Paragraph 4 of Section 9.6.2 of EGR-NGGC-0203 discussed the

determination of actual valve factor in the reconciliation of

dynamic test data. The inspectors noted that the determination of

a valve factor from test data up to the point of flow isolation

will be difficult to apply to other valves because of design and

manufacturing tolerances. The inspectors also noted that the use

of valve inlet pressure when the valve is fully closed (rather

than pressure at flow isolation) might result in underestimation

of the valve factor determined for the point of flow isolation.

The inspectors noted similar guidance provided in Paragraph 5 of

Section 9.6.2 on thrust extrapolation.

Paragraph 5 of Section 9.6.2 of EGR-NGGC-0203 discussed the

extrapolation of the thrust requirements from dynamic test data to

16

higher differential-pressure conditions. A note in this paragraph

specified a minimum test differential pressure of 80% of the

design-basis value. The note referenced guidance from the

Electric Power Research Institute (EPRI) on the extrapolation of

test data, but did not discuss the minimum absolute value of

contact load considered in the EPRI guidance. In response to

inspectors' questions regarding this condition, the licensee

performed a preliminary evaluation to ensure that no present

concerns existed with the extrapolation of test data at Robinson.

Paragraph 6 of Section 9.6.2 of EGR-NGGC-0203 provided guidance on

the calculation of thrust margin for an MOV to perform its safety

function. The inspectors noted that diagnostic error was not

considered. The licensee personnel indicated that the guidance

would be removed or revised to resolve this concern.

The licensee provided guidance for the calculation of motor output

torque for ac-powered and dc-powered MOVs in Procedure EGR-NGGC-0101.

The licensee was also preparing ESR-9700380 to provide guidance on

determining torque output for MOVs. The inspectors noted that these

documents indicated that the effect of ambient temperature on motor

torque output would be considered. The inspectors identified these

documents for further review, including consistency with guidance from

the manufacturer on ambient temperature effects on actuator output,

during a closure inspection for GL 89-10.

Valve Factor and Groupings

In Inspection 50-261/96-12, the NRC found that the licensee had not

adequately justified the valve factor assumptions which it used in

determining thrust and torque requirements for valves that had not been

dynamically tested. This was considered to represent inadequate design

control and was identified as Example 1.a of Violation 50-261/96-12-05,

Unjustified Design Assumptions and Incorrect Stem Rejection Load. In

developing its response to this violation, the licensee had prepared

ESR-9700330 to separate GL 89-10 valves into groups based on valve

manufacturer, model, size, seat, guide, wedge, disc materials, design

basis conditions, and installation configuration. In ESR-9700330, the

licensee established 16 groups for its GL 89-10 gate valves. The

licensee established only one group for its GL 89-10 globe valves

because all five valves were Velan 2-inch globe valves. The licensee

considered the three Allis Chalmers 16-inch butterfly valves in its GL 89-10 program also as one group. The licensee was justifying valve

factors for non-dynamically tested gate and globe valves based on test

data from other valves in the applicable group or from outside sources,

or on thrust and torque predictions that were being calculated using the

EPRI MOV Performance Prediction Methodology (PPM).

The licensee indicated that its justification for valve factors and

grouping had not been completed. The inspectors considered the

licensee's ongoing approach to be consistent with the intent of GL 89-10

and its supplements. The NRC will perform a final review during a

17

future closure inspection for GL 89-10. From their current review, the

inspectors identified concerns for evaluation during that inspection:

For some valve groups, the licensee indicated that the highest

valve factor obtained from dynamic testing of valves in the group

would be applied to other non-dynamically tested valves in that

group. It was not clear that the licensee had reviewed the test

data to ensure that the valve factor selected as the design value

for the group was consistent with the potential statistical

variation of the valve factors determined from the tested valves.

For some valve groups, the licensee indicated that the valves had

only to provide flow isolation rather than a leak-tight seal. As

already mentioned above, the thrust requirements to achieve flow

isolation are difficult to apply from one valve to another because

of design and manufacturing tolerances. Further, in Inspection

Report 50-261/96-12, the inspectors described the difficulty

experienced by licensee personnel in conservatively selecting the

point of flow isolation in the dynamic data trace for MOV AFW-V2

14A, Steam Drive Auxiliary Feed Water Pump Discharge Valve to

Steam Generator A. The inspectors also questioned whether the

licensee had reviewed the flow requirements for each valve in

these groups to ensure that a thrust requirement to achieve only

flow isolation was applicable to the valves.

The licensee initially indicated that the actual valve factor

determined from a dynamic test of some valves might be applied in

establishing the design thrust and torque requirements for those

valves. The inspectors were concerned that this might result in

the selection of a valve factor that was too low. They noted that

valve factors for MOVs can increase with age and service, as

observed in repetitive dynamic tests performed on certain of the

licensee's valves. Where the assumed valve factor (or other

parameters, such as load sensitive behavior or stem friction

coefficient) for a valve is based on a specific MOV test, small

changes in MOV performance may result in the need to evaluate MOV

operability and update the valve's setup calculations. Licensee

personnel indicated that conservative minimum design valve factors

would be selected to help address this concern.

The inspectors noted that the licensee was relying on EPRI

separate effects data and test results from double disc valves to

justify the valve factor used for two Copes Vulcan 14-inch

parallel disc gate valves (in

Group DD7). The inspectors

questioned whether this information was sufficient for these

valves. Licensee personnel indicated that the safety function of

these valves and the justification for the design valve factor

were still under evaluation.

The inspectors questioned the limited test data from another

facility that was relied on in justifying the design valve factor

for the Power Operated Relief Valve Block Valves at Robinson.

18

Licensee personnel indicated that use of the EPRI MOV PPM was

being considered to help justify the thrust requirements for these

valves.

The licensee relied on test data from the EPRI MOV test program to

justify a design valve factor of 1.1 for its globe valves. The

inspectors were concerned that the EPRI data might not be

applicable to the licensee's valves and noted that more

appropriate data might be available from other industry sources.

During Inspection 50-261/96-12, the inspectors found that the then

current version of EGR-NGGC-0203 (Revision 0) provided an incorrect

equation for calculating valve factor in the opening valve direction.

At that time, the inspectors also found the dynamic test evaluation

packages for several MOVs used this equation and incorrectly calculated

the open valve factor. The licensee's incorrect calculation of opening

valve factors was identified as Example 2 of Violation 50-261/96-12-05.

In the current inspection, the inspectors verified that the licensee had

corrected the equation in EGR-NGGC-0203, Revision 3. The licensee was

presently updating the dynamic test reconciliation data packages which

might have used the equation. The NRC will review the calculation of

open valve factor for specific valve tests during a GL 89-10 future

inspection.

Load Sensitive Behavior

During Inspection 50-261/96-12, the inspectors found that the licensee

had not adequately justified its assumption for load sensitive behavior.

This was considered to represent inadequate design control and was

identified as Example 1.b of Violation 50-261/96-12-05. In response,

the licensee prepared ESR-9700328 to justify the load sensitive behavior

assumed for MOVs not dynamically tested at Robinson. Using test data

from 13 gate valves at Robinson, the licensee calculated load sensitive

behavior as the ratio of the thrust at static torque switch trip minus

the thrust at dynamic torque switch trip to the thrust at dynamic torque

switch trip. Typically in the industry, the thrust at static torque

switch trip is used in the denominator for this calculation. The

licensee statistically analyzed the load sensitive behavior data and

determined that the mean was 5.6% and two standard deviations were

23.8%. The licensee found that the load sensitive behavior determined

for Robinson compared favorably with that determined for its other

plants and to the values obtained by EPRI using the same lubricant.

The licensee did not have dynamic test data from its globe valves for

use in determining their load sensitive behavior. In ESR-9700328, the

licensee analyzed information from globe valve testing by EPRI. Based

on its analysis, the licensee determined a mean value of load sensitive

behavior of 12.4% and a two standard deviation value of 18.6% for its

globe valves at Robinson.

The licensee indicated that load sensitive behavior would only be

applied in calculations for torque switch controlled operation. In ESR-

19

9700328, the licensee indicated that the stem friction coefficient

obtained under dynamic conditions would be applied in situations where

MOVs were controlled by limit switch setting.

The inspectors found that the approaches used by the licensee in

determining and justifying load sensitive behavior values were generally

satisfactory. The NRC will further evaluate the values selected and

their application in a future GL 89-10 closure inspection.

Stem Friction Coefficient

During Inspection 50-261/96-12, the inspector found that the licensee

had not adequately justified the stem friction coefficient assumed in

the MOV setting calculations at Robinson. This failure to justify stem

friction coefficient represented inadequate design control, which was

identified as Example 1.c of Violation 50-261/96-12-05. During the

current inspection, the inspectors found that the licensee was preparing

ESR-9700331 to establish appropriate assumptions for stem friction

coefficients at Robinson. The licensee had not completed its

justification during this inspection.

MOV Setup Calculations

The inspectors found that the licensee was updating the setup

calculations for its GL 89-10 MOVs to address the findings of a recent

self-assessment and an NRC inspection at its Brunswick facility.

Design-Basis Capability

During Inspection 50-261/96-12, the inspector reviewed the results of

tests which the licensee performed to establish the design basis

capabilities of its valves. In three examples, the licensee's

evaluations of these test results were found inadequate. These examples

were considered to represent inadequate test control and were cited in

Violation 50-261/96-12-06:

Inadequate Evaluation of Test Results.

During the current inspection the inspectors found that the licensee was

addressing the violation examples as follows in (corporate) Procedure

EGR-NGGC-0203:

Example 1 involved failures to recognize that the dynamic test

results were not consistent with the perceived test conditions.

Further, the test procedures did not ensure that the intended

design-basis test conditions were achieved during the tests. In

response to the violation, the licensee provided guidance in

Section 9.6 of EGR-NGGC-0203 to help improve the adequacy of MOV

diagnostic tests. The inspector will review the licensee's

evaluations of specific MOV diagnostic tests relative to this

violation example during a future inspection.

Example 2 involved the licensee's failure to adjust open thrust

measurements to account for measurement uncertainty identified by

the licensee's VOTES diagnostic equipment vendor, Liberty

20

Technologies, in its Customer Service Bulletin 31 (dated

November 19, 1993). In response to the violation, the licensee

revised EGR-NGGC-0203 in Section 9.1.3 to address the

consideration of VOTES diagnostic measurement uncertainty in

accordance with the applicable vendor guidance and customer

service bulletins.

Example 3 involved the licensee's failure to evaluate the

significance of a severe anomaly in the diagnostic trace of a

dynamic test of MOV MS-V1-8B, Steam Generator B Steam Supply to

Steam-Driven AFW Pump. In response, the licensee revised EGR

NGGC-0203 to improve the evaluation of diagnostic test data. The

inspector will review the adequacy of the licensee's evaluation of

specific MOV diagnostic test results during a future inspection.

The licensee also responded to the above violation examples through

changes to the Robinson plant procedures and other actions, as described

in Section E8.2 of this report.

The inspectors considered the licensee to be addressing the findings and

violation on the performance of MOV tests and the evaluation of MOV test

results identified in Inspection Report No. 50-261/96-12. The inspector

plans to complete his review during a future inspection.

In this inspection, the inspectors noted that the licensee's

determination of available capability revealed several MOVs to have

negative margin in their non-safety directions. In response to

inspectors' questions, the licensee prepared preliminary evaluations to

demonstrate no concern with the performance of the safety function of

these MOVs despite the negative margin.

2. Periodic Examination of MOV Data for Trends

Requirements for periodic examination of MOV data for trends were

described in Technical Management Manual Procedure TMM-032, "Motor

Operated Valve Program," Revision 9. This procedure required

documentation of a periodic review of maintenance and test data at least

every two years. The inspectors found that the licensee issued detailed

periodic trend reports of MOV maintenance and testing information every

two years and trend reports of MOV failures and problems every six

months. The following examples of the reports were verified by the

inspectors:

Trending of MOV Maintenance and Testing Information Reports dated

July 7, 1995 and May 1, 1997

MOV Maintenance Trending Reports for July 1 through December 31,

1996 and January 1 through June 30, 1997

The inspectors reviewed the database compiled by the licensee for the

period of October 1996 to October 1997 and found that the entries in the

database and the evaluations presented in the trend reports were

21

consistent. The recommendations of GL 89-10 for trending were

satisfactorily implemented. The inspectors found no evidence of adverse

trends in the performance of Robinson GL 89-10 valves for the period.

c. Conclusions

The licensee had not met its original commitment date for correcting

adverse findings regarding its implementation of GL 89-10 identified

during Inspection 50-261/96-12. Progress toward correcting the findings

by the new date proposed by the licensee was generally satisfactory.

Some concerns were identified, as described above. These concerns and

the outstanding findings from Inspection 50-261/96-12 will be re

examined in a future inspection which will assess the licensee's

completion of GL 89-10 implementation.

E7

Quality Assurance in Engineering Activities

E7.1 Motor-Operated Valve Program Self-Assessment (TI 2515/109)

An assessment of the Robinson MOV program was completed in August 1997

by the licensee's Nuclear Assessment Section (NAS) and was documented as

Report File No. R-ES-97-01. From a review of the assessment report, the

inspectors found that the assessment had been thorough and had resulted

in important findings. Several findings were similar to findings

independently identified by the inspectors. The inspectors verified

that the findings were appropriately identified for resolution by the

licensee in CRs 97-01822, -01824, and -01848. The corrective actions

had been or were being scheduled and licensee personnel stated that a

matrix describing the status of the NAS assessment findings would be

prepared.

7.2

Special UFSAR Review (37551)

A recent discovery of a licensee operating their facility in a manner

contrary to the UFSAR description highlighted the need for a special

focused review that compares plant practices, procedures and/or

parameters to the UFSAR descriptions. While performing the inspections

discussed in this report, the inspector reviewed the applicable portions

of the UFSAR related to the areas inspected. The inspector verified

that for the select portions of the UFSAR reviewed, the UFSAR wording

was consistent with the observed plant practices, procedures and/or

parameters.

E8

Miscellaneous Engineering Issues (92903)

E8.1

(Open) Violation (VIO) 50-261/96-12-05, Unjustified Design Assumptions

and Incorrect Stem Rejection Load: This violation identified that

important assumptions used in setting and capability calculations had

not been justified and that calculations used in determining opening

valve factors contained errors involving the stem rejection loads

selected. Section E1.2 describes the licensee's response letters and

schedule to resolve this violation and discusses some of the corrective

22

actions that had been taken. The inspectors found that the related

corrective actions identified by the licensee were specified in CR 96

03179. The corrective actions and the inspectors' findings as to the

status of each were as follows:

(1) Corrective action:

Review past test evaluations and procedures.

Then, based on the results of the review, revise set-up and

reconciliation calculations.

Inspectors' findings: The licensee had reviewed past test

evaluations and procedures. As discussed in E1.2, the inspectors

found that the licensee was preparing justifications for the

assumptions used in its set-up and reconciliation calculations and

that the calculations were in revision. The assumption

justifications and revisions to the set-up and reconciliation

calculations will be evaluated in a future inspection.

(2) Corrective action: Revise procedural guidance for calculating

opening valve factors and train personnel on the revision.

Correct previous calculations.

Inspectors' findings: The inspectors reviewed the applicable

procedure, EGR-NGGC-0203, and verified that it had been revised to

provide the correct guidance. This involved specifying use of an

appropriate equation for the calculation, as described in E1.2

above. The inspectors also verified licensee documentation of

training on the revised procedure, which was recorded on a

training report dated May 30, 1997. The inspector plans to verify

correct application of the revised guidance during a future

inspection.

(3) Corrective Action: Perform a self-assessment of the MOV program by

September 29, 1997.

Inspectors' findings: The self-assessment had been satisfactorily

completed, as discussed in E7.1.

E8.2 (Open) Violation 50-261/96-12-06, Inadequate Evaluation of Test Results:

This violation identified that the licensee had not adequately evaluated

certain test data. The licensee had not adjusted valve opening thrust

measurements for test measurement error, failed to recognize that test

data indicated that the test conditions in some tests were not as

intended, and failed to resolve significant anomalies exhibited in some

test data. Section E1.2 describes the licensee's response letters and

schedule to resolve this violation. The inspectors found that the

related corrective actions identified by the licensee were specified in

CR 96-03178. The corrective actions and the inspectors' findings as to

the status of each were as follows:

(1) Corrective action: Revise procedures to require documentation of

the acceptability of test parameters, an MOV engineer's presence

23

and preliminary review of each dynamic test at the test location,

and consideration of extrapolation error.

Inspectors' findings: The inspectors verified the procedure

changes had been incorporated into Robinson Procedures TMM-032,

Revision 9 and TMM-035, Revision 11.

(2) Corrective action:

Review previous MOV test evaluations to verify

the accuracy of the test parameters used in reconciliation

calculations. Revise set-up and reconciliation calculations based

on the findings of the review.

Inspectors' findings: The inspectors verified that the licensee

had completed the review of previous MOV test evaluations and

documented the results in Technical Report No. 97111-TR-01,

Revision 1. Set-up and reconciliation calculation revisions were

still in process. Appropriate revisions to set-up and

reconciliation calculations will be verified during a future

inspection.

(3) Corrective action: Conduct classroom training of MOV personnel on

interpretation of test data by September 29, 1997. Perform

additional training during the Spring 1998 refueling outage.

Inspectors' findings: The inspectors verified records of

completion of the initial classroom training, including test

scores. These were documented in a letter to the licensee dated

September 23, 1997, from the contractor (Liberty Technologies)

that conducted the training.

(4) Corrective action: Revise MOV program controls to require

periodic program assessments utilizing industry experts. Conduct

a self-assessment of the MOV program by September 29, 1997.

Inspectors' findings: The inspectors verified that requirements

for periodic program assessments were included in Procedure TMM

032, Revision 9. The assessments were specified to be performed

annually by MOV program experts. The self-assessment had been

completed, as discussed in E7.1.

In addition to the above corrective actions, which specifically

addressed the Robinson plant, the licensee also provided changes to a

corporate procedure (EGR-NGGC-0203), as described in E1.2 of this

report.

E8.3 (Closed) URI 50-261/97-08-02, Review Root Cause of Increased Containment

Air Temperature: This URI involved the unexpected increase in

containment average air temperature experienced between June and August

of 1997. The licensee initially implemented several initiatives to

lower containment air temperature, including; starting an additional

service water cooling pump, starting additional control rod drive

mechanism cooling fans and containment air iodine removal exhaust fans.

24

These actions had marginal impact on reducing temperatures. On July 5,

1997, the volumetrically weighted average calculation of containment air

temperature indicated that the temperature had increased slightly above

the 120oF containment design basis limit, resulting in the licensee

reporting to the NRC, a condition outside design basis. Immediate

actions were implemented to perform a containment purge to reduce

containment temperature below 120 0F. Later, continuous containment dome

cooling was implemented, as well as a pump installed to transfer water

from a cooler portions of the lake directly to the suction of the

service water intake structure. As a result of these initiatives, the

licensee was able to continue operation at full power during the hot

period of the summer without exceeding 120oF.

The containment average air temperature is an initial condition used in

the licensee's design basis accident analyses that establishes the

containment environmental qualification and operating envelope for both

pressure and temperature. The 120oF design limit ensures that operation

is maintained within the assumptions used in the design basis analyses.

UFSAR Section 9.4.3.1 states, in part, that one of the design functions

of the Containment Building Ventilation System is to remove the normal

heat lost from all equipment and piping in the reactor containment

during plant operation and maintain a temperature of 120'F or less

inside the containment, with 950F cooling water and three-out-of-four

Containment Air Recirculation Cooling (CARC) fans operating.

The inspector reviewed modification package ESR 9500783, which was

implemented during the previous (RFO 17) refueling outage.

Additionally, the inspector reviewed CR 97-01471, which was initiated by

the licensee to investigate the increased containment temperature. The

modification changed the normal power operation alignment of the four

CARC fan units, HVH-1, 2, 3, and 4. Specifically, the normal air intake

dampers were secured in the closed position and the emergency intake

butterfly valve dampers were secured in the open position. Previously,

during normal power operations, the normal intake dampers were

positioned open and the emergency intake dampers were closed. Following

a Safety Injection (SI) actuation, prior to the modification, the normal

dampers would close and the emergency dampers would open. Following the

modification, the damper positions would not change following an SI,

(i.e., the normal dampers would stay closed and the emergency dampers

would stay open).

The inspector noted several inadequacies in the licensee's

implementation of modification ESR 9500783. On October 11, 1996,

partial turnover of the modification was performed following completion

of air flow measurements. The CARC system was declared operable at that

time. However, from review of modification test data results, on

July 15, 1997 the inspector noted that only 245,133 cubic feet per

minute (cfm) of total air flow was measured with all four CARC units

operating, while the test acceptance criteria specified a minimum of

255,000 cfm. At that time, a note was written next to these steps,

indicating that the lower flow was acceptable due to flow measurement

instrument tolerances. The inspector considered the documentation of

25

these steps to have been untimely, and the note was not adequate

documentation for resolving the failure to meet the test acceptance

criteria.

The design review also did not consider that four CARC units were

necessary to maintain temperatures below 120 0F in the hot periods of the

summer during normal operations, as opposed to three, as stated in UFSAR

Section 9.4.3.1. The modification should have recognized this and

appropriately updated the UFSAR section to accurately reflect the plant

configuration requiring four CARC units maintain temperatures below

120 0F. The aforementioned UFSAR section had existed prior to the

modification, and the modification presented an opportunity to address

this inconsistency, but was not recognized by the licensee.

Additionally, it was expected that the modification in damper alignment

at power would result in enhanced cooling performance from the CARC

units. The modification erroneously assumed that air flow through the

cooling coils would be more evenly distributed as compared to the

original configuration. The change actually had an opposite effect,

resulting in less cooling capability of the CARC units. The

modification package had indicated that appropriate testing would be

performed to assure that the air flow as well as cooling performance of

the system during normal power operation would be equal to the original

Design Basis. However, post modification testing consisted of only

measuring the air flow through the system with all four CARC units

operating concurrently, and not the cooling performance testing.

The

measurement of air flow alone was not sufficient to confirm the cooling

performance of the CARC units nor the assumption that the cooling

performance would be improved. Thus, the cause of the elevated

containment temperatures stemmed from the implementation of modification

ESR 9500783 during the previous refueling outage. The normal cooling

capability of the CARC system at power was adversely impacted due to

uneven air flow distribution across the cooling coils of the CARC units.

10 CFR 50, Appendix B, Criterion V, Instructions, Procedures, and

Drawings, requires in part that activities affecting quality shall be

prescribed by documented instructions and shall be accomplished in

accordance with these instructions. Further, the instructions shall

include quantitative or qualitative acceptance criteria for determining

that important activities have been satisfactorily accomplished.

The inspector determined that when post modification test acceptance

criterion was not met, an evaluation was not conducted prior to

declaring the CARC system operable. The failure to follow procedure as

required .by procedure EGR-NGGC-005 was a violation of 10 CFR 50,

Appendix B, Criterion V. This is identified as example 1 of violation

50-261/97-12-04: Failure to Accomplish Modification Related Activities

for the Containment Air Recirculation Cooling System. Further, the

modification package indicated that appropriate testing would be

performed to assure that the air flow as well as cooling performance of

the system would be equal to the original Design Basis. However, the

post modification test for ESR 9500783 did not evaluate the cooling

26

capability following the modification to confirm that the system was

capable of meeting its Design Basis during normal plant operations. The

failure to follow the modification package requirements is identified as

example 2 of violation 50-261/97-12-04.

E8.4 (Closed) URI 50-261/96-14-03, Review Aspects of Containment Spray

Additive Tank Eductor Line Sampling: This URI involved inspector

concerns with the adequacy of the licensee's 10 CFR 50.59 evaluation

associated with procedures for conducting quarterly sampling/flushing of

the sodium hydroxide eductor piping associated with the Containment

Spray System (CSS). In order to conduct the sampling/flushing

activities, the spray additive tank eductor piping was aligned in a

configuration that degraded its design function of automatically

providing sodium hydroxide to the suction of both CSS pumps. Instead of

declaring the sodium hydroxide addition system inoperable, credit was

taken for manual operator actions to restore the eductor piping to its

automatic alignment within six minutes in the event of a CSS actuation

signal.

The six minutes was based on the results of a licensee

calculation that indicated the effect of this delay in sodium hydroxide

addition to the containment atmosphere during a design basis accident

would not result in exceeding General Design Criteria (GDC) 19 or 10 CFR

100 dose limits.

In the previous inspection, the inspector questioned the adequacy of the

safety evaluations which supported these procedure changes, in that, the

evaluations appeared to involve an unreviewed safety question. The

procedures introduced two new failure modes for the iodine removal

system, which both, increased the possibility for malfunction of a

different type than any evaluated in the UFSAR. These new failure modes

involved the potential malfunction of manual valves that the operator's

were dedicated to open which were previously in an open position, and

the potential failure of the operators to perform the manual realignment

within the time allowed. The failure to return the system to its

automatic alignment due to either of the above reasons within six

minutes could have resulted in the failure of the iodine removal system

from performing its intended safety function. In addition, the

licensee's calculation to support the six minute delay indicated that

the GDC 19 dose limits would increase from 27.3 rem to 29.7 rem. This

was very close to the GDC 19 limit of 30 rem.

The licensee had previously indicated that they believed that guidance

in NRC Inspection Manual Chapter, Part 9900, Interim Guidance on 10 CFR

50.59, issued in April 1996, and Generic Letter 91-18, Information to

Licensees Regarding Two NRC Inspection Manual Sections on Resolution of

Degraded and Nonconforming Conditions and on Operability, allowed the

substitution of manual action for automatic action.

As a result of the inspector's concerns regarding the sampling/flushing

activities, the licensee initiated Engineering Service Request (ESR)

9700050 to evaluate whether the practice should be continued. The

results of this evaluation indicated that, since 1991, there had not

been any evidence of leakage past the Spray Additive Tank Isolation

27

Valves, SI-845A&B; therefore, it was recommended that the

sampling/flushing activity be discontinued. Based on the results of ESR

970050, the sampling/flushing activities were removed from operations

surveillance procedures (OST-352-1 and -2) associated with the CSS that

were conducted at power operation.

The inspector noted that the NRC has recognized that better regulatory

guidance is needed to ensure the consistent implementation of 10 CFR

50.59, including such areas as, the use of compensatory measures to

offset small potential increases in probabilities, as well as defining

when reductions in the margin of safety are evident. Based on

discussions with licensee engineering and licensing personnel,

additional training to personnel conducting 10 CFR 50.59 safety

evaluations had been provided since the time that the inspector

initially identified this problem. The inappropriate crediting of

operator action in lieu of automated actuations had been specifically

addressed during this training.

The licensee was in the process of enhancing their 10 CFR 50.59 program

by the addition of a Design Review Panel and PNSC Safety Evaluation

Subcommittee. The purpose of the panel and subcommittee was to review

all 10 CFR 50.59 evaluations and a sample of evaluation screens to

ensure adequacy and adherence with procedures and guidance.

Additionally, procedures related to the implementation of 10 CFR 50.59

were scheduled to be revised in December 1997 to provide better 10 CFR

50.59 guidance, especially in the area related to compensatory measures

and margin of safety. Based on the licensee's completed and planned

actions to enhance their 10 CFR 50.59 program, and the licensee's

revision of procedures deleting the sampling/flushing activities, this

URI is closed.

IV. Plant Support

R1

Radiological Protection and Chemistry Controls

R1.1 General Comments (71750)

The inspector periodically toured the Radiological Control Area (RCA)

during the inspection period. Radiological control practices were

observed and discussed with radiological control personnel including RCA

entry and exit, survey postings, locked high radiation areas, and

radiological area material conditions. The inspector concluded that

radiation control practices were proper.

28

S1

Conduct of Security and Safeguards Activities

S1.1 General Comments (71750)

During the period, the inspector toured the protected area and noted

that the perimeter fence was intact and not compromised by erosion nor

disrepair. Isolation zones were maintained on both sides of the barrier

and were free of objects which could shield or conceal an individual.

The inspector periodically observed personnel, packages, and vehicles

entering the protected area and verified that necessary searches,

visitor escorting, and special purpose detectors were used as applicable

prior to entry. Lighting of the perimeter and of the protected area was

acceptable and met illumination requirements.

V. Management Meetings

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee

management at the conclusion of the inspection on December 3, 1997. No

proprietary information was identified.

29

PARTIAL LIST OF PERSONS CONTACTED

Licensee

J. Boska, Manager, Operations

H. Chernoff, Supervisor, Licensing/Regulatory Programs

T. Cleary, Manager, Maintenance

J. Clements, Manager, Site Support Services

J. Keenan, Vice President, Robinson Nuclear Plant

R. Duncan, Manager, Robinson Engineering Support Services

R. Moore, Manager, Outage Management

J. Moyer, Manager, Robinson Plant

R. Warden, Manager, Nuclear Assessment Section

T. Wilkerson, Manager, Regulatory Affairs

D. Young, Director, Site Operations

NRC

B. Desai, Senior Resident Inspector

J. Zeiler, Resident Inspector

30

INSPECTION PROCEDURES USED

IP 37551:

Onsite Engineering

IP 40500:

Effectiveness of Licensee Controls in Identifying, Resolving, and

Preventing Problems

IP 61726:

Surveillance Observations

IP 62700:

Maintenance Implementation

IP 62707:

Maintenance Observation

IP 71707:

Plant Operations

IP 71714:

Cold Weather Preparations

IP 71750:

Plant Support Activities

IP 92901:

Followup - Operations

IP 92902:

Followup - Maintenance

IP 92903:

Followup - Engineering

IP 93702:

Prompt Onsite Response to Events at Operating Power Reactor

T12515/109: Inspection Requirements for Generic Letter 89-10, Safety-Related

Motor-Operated Valve Testing and Surveillance

ITEMS OPENED,

CLOSED,

AND DISCUSSED

Opened

Type

Item Number

Status

Description and Reference

NCV

50-261/97-12-01

Open

Failure to Log TS Surveillance Completion

in Accordance with OST-020 (Section 01.3)

NCV

50-261/97-12-02

Open

Failure to Verify Dose Equivalent 1-131 in

Accordance with GP-005 (Section 01.3)

IFI

50-261/97-12-03

Open

Review Safety Injection Discharge Piping

Configuration (Section E1.1)

VIO

50-261/97-12-04

Open

Failure to Accomplish Modification Related

Activities for the Containment Air

Recirculation Cooling System

(Section E8.3)

Closed

]Iype

Item Number

Status

Description and Reference

NCV

50-261/97-12-01

Closed

Failure to Log TS Surveillance Completion

in Accordance with OST-020 (Section 01.3)

NCV

50-261/97-12-02

Closed

Failure to Verify Dose Equivalent 1-131 in

Accordance with GP-005 (Section 01.3)

URI

50-261/97-10-01

Closed

Complete Review of LPMS Testing and

Maintenance Activities (Section 08.1)

31

URI

50-261/97-08-02

Closed

Review Root Cause of Increased Containment

Air Temperature (Section E8.3)

URI

50-261/96-14-03

Closed

Review Aspects of Containment Spray

Additive Tank Eductor Line Sampling

(Section E8.4)

Discussed

13pe

Item Number

Status

Description and Reference

VIO

50-261/96-12-05

Open

Unjustified Design Assumptions and

Incorrect Stem Rejection Load (Section

E8.1)

VIO

50-261/96-12-06

Open

Inadequate Evaluation of Test Results

(Section E8.2)