ML14181A872

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Integrated Insp Rept 50-261/96-14 on 961117-1228.Violations Noted.Major Areas Inspected:Licensee Operations,Maint, Engineering & Plant Support
ML14181A872
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 01/17/1997
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14181A869 List:
References
50-261-96-14, NUDOCS 9702110129
Download: ML14181A872 (45)


See also: IR 05000261/1996014

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket No:

50-261

License No:

DPR-23

Report No:

50-261/96-14

Licensee:

Carolina Power & Light (CP&L)

Facility:

H. B. Robinson Unit 2

Location:

2112 Old Camden Rd.

Hartsville, SC 29550

Dates:

November 17 - December 28, 1996

Inspectors:

B. Desai, Senior Resident Inspector

J. Zeiler, Acting Senior Resident Inspector

P. Byron, Resident Inspector, Surry

F. Jape, Project Engineer, RII (Section 07.2)

G. MacDonald, Project Engineer, RII (Section

07.2)

J. Lenahan, Reactor Inspector, RII (Sections

07.2, El, E2, ES, and E7)

G. Salyers, Reactor Inspector, RII (Sections P2,

P3, P5, P6, and P7)

Approved by:

M. Shymlock, Chief, Projects Branch 4

Division of Reactor Projects

Enclosure 2

9702110129 970117

PDR

ADOCK 05000261

G

PDR

EXECUTIVE SUMMARY

H. B. Robinson Power Plant, Unit 2

NRC Inspection Report No. 50-261/96-14

This integrated inspection included aspects of licensee operations,

maintenance, engineering, and plant support. The report covers a six-week

period of inspection. In addition to inspections conducted by resident

inspectors, it includes the results of an engineering inspection conducted by

a regional inspector, an emergency preparedness inspection conducted by a

regional inspector, and, a corrective action program inspection conducted by

regional project engineers and inspectors.

Operations

Operations personnel demonstrated a heightened sensitivity to potential

hydraulic transients with the identification of a water hammer during

startup of the C Auxiliary Boiler. Engineering performed a detailed

investigation of the transient and were successful in identifying the

root cause. Licensee planned corrective actions were appropriate to

address the procedure discrepancy identified, as well as the generic

implications of other potential procedural configuration weaknesses.

The inspectors noted that continued licensee emphasis and sensitivity to

potential hydraulic transients was warranted due to past weaknesses in

this area (Section 01.2).

Operators responded appropriately-upon noting the abnormal condition

relative to water dripping into an Emergency Diesel Generator room from

a crack in the concrete roof. The licensee adequately evaluated the

safety impact of the crack on the operability of diesel generator

(Section 01.3).

A failure of an instrument air tubing caused a Feedwater Heater level

controller to fail resulting in a transient and a subsequent power

reduction. Further, it was identified that Feedwater Heater relief

valves were not in a periodic testing program. The decision to restore

the 6A Feedwater Heater to normal alignment at full power was considered

a weakness. Continued licensee attention relative to the reliability of

the Instrument Air System, as well as periodic testing of secondary

relief valves is warranted (Section 01.4).

The onsite review functions of the Plant Nuclear Safety Committee (PNSC)

were conducted in accordance with Technical Specifications. The PNSC

meeting attended by the inspectors was well coordinated and meeting

topics were thoroughly discussed and evaluated (Section 07.1).

Based on review of selected Conditions Reports (CRs), it was concluded

that the licensee's corrective action management program was being

implemented in accordance with licensee procedures and regulatory

requirements (Section 07.2).

In general, personnel in all organizational components were identifying

and fixing problems within their area. CRs were discussed on a regular

basis and being assigned for action. CR assessments were thorough and

2

root causes analyses were considered good. Trending of CR data by unit

managers was an effective method for identifying and reversing problems

and adverse trends, and improve overall plant performance (Section

07.2(1)).

Several potential adverse conditions were voided with poor documentation

of justification. A need for training was indicated by the number of

voided CRs with poor documentation of justification. The large number

of voided CRs also indicated a weakness in personnel awareness of what

constituted an adverse condition (Section 07.2(1)).

Self-assessments in Engineering, and Materials and Contract services

indicated a need for training. Nuclear Assessment Section assessment

96-01 identified a weakness in the understanding of the CR process..

Discussions with plant personnel disclosed that there was no formal

training provided to personnel, other than CR evaluation personnel

(Section 07.2(1)).

The Operating Experience Program (OEP) was judged to be effective. The

completed OE evaluations reviewed were acceptable. OEP self-assessments

and NAS audits were thorough. The OE weekly status meeting, monthly

report, and OE tracking provided good program oversight. The

incorporation of OE data into routine daily activities was viewed as a

strength (Section 07.2(2)).

The self-assessment program has been effective in identifying

performance deficiencies and was useful in providing oversight to

management. Managers have been proactive in following up on issues

identified at other sites to identify and correct deficiencies at the

plant. Licensee management is committed to the self-assessment process

as indicated by the resources, including assistance of outside

organizations, involved in the self-assessment process, and the number

of self-assessments performed on an annual basis (Section 07.2(3)).

Operations personnel identification and response to an anomaly between

Steam Pressure transmitter output and energization of Freeze Protection

circuitry was considered an example of good attention to detail and

plant monitoring (Section M1.2).

Maintenance

The inspectors concluded that maintenance and surveillance activities

were performed satisfactorily (Section M1.1).

The lack of comprehensive preventive maintenance on the Freeze

Protection system was identified as a weakness in the licensee's cold

weather protection program. Had there been preventative maintenance to

verify the operability of Freeze Protection system thermostats, the

problems associated with thermostats in the Steam Generator and Steam

Header pressure transmitter cabinets could have been identified

previously (Section M1.2).

3

Engineering

The licensee's design change process was determined to be adequate,

however, a concern was identified that a process was in place that used

an engineering review in lieu of a design verification for plant changes

designated as configuration changes only. An Unresolved Item (URI) was

identified for further review of the licensee's engineering review

requirements. The existence of duplicate administrative procedures

(corporate and site specific) controlling the engineering design and

design change process could result in confusion and design control

errors in the future due to differences in requirements (Section E1.1).

Design changes and modification packages reviewed were determined to be

of good quality. The packages contained sufficient specifications,

drawings, and procedures to be properly installed and tested (Section

E1.2).

A violation was identified regarding the licensee's failure to follow

procedures in canceling corrective actions required by an engineering

evaluation for inspections of the containment liner plate for corrosion

(Section E2).

Engineers were actively involved in the day-to-day support of plant

equipment. The material condition of the plant and equipment was

considered good to excellent (Section E2).

The licensee's program for training and qualification of system

engineers was determined to meet regulatory requirements (Section E5).

An Unresolved Item was identified involving a potential inadequate

10CFR50.59 evaluation conducted for a change to a procedure allowing the

Containment Spray System to be aligned in an undesirable configuration

during Spray Additive Tank discharge valve leakage testing (Section

E8.1).

Engineering thoroughly evaluated Steam Generator and Steam Header

pressure transmitter output anomalies that were caused from higher than

designed cabinet temperatures resulting from Freeze Protection system

malfunctions (Section M1.2).

Plant Support

The Emergency Preparedness (EP) program was receiving strong management

support (Section P6). The EP facilities were satisfactorily equipped

and maintained in operational readiness (Section P2.1). The operational

status and maintenance of the siren system was good (Section P2.3).

The

licensees's dose assessment capabilities were satisfactory and

sufficient personnel were trained to perform onshift dose assessment

using real time meteorological and radiological data (Section P2.2).

The new designation and reorganization of the EP procedures was

considered an improvement (Section P3.1).

4

The licensee was effectively implementing the Emergency Response

Organization training program. The licensee had rewritten their

training program and reorganized their lesson plans. The new training

program and lesson plan were an improvement, but the exams could be

improved (Section P5.2).

Combining licensed operator retraining with

emergency preparedness drills was a strength for the emergency

preparedness program and resulted in an increase in the number of

training drills (Section P5.1). The number of drills performed during

the year, the level of participation, and the feedback training provided

to the players was a strength (Section P5.3).

Nuclear Assessment Section audits of the EP program were detailed in

scope and thorough (Section P7.1).

The EP organization was adequately tracking and resolving upper tier

issues. The licensee's loss of their lower level tracking system for EP

drill comments and issues contributed to continuing problems with

documentation. Control of documentation continues to be a concern

(Section P7.2).

Report Details

Summary of Plant Status

Unit 2 remained at power the entire inspection period completing 70 days of

continuous operation since startup from Refueling Outage 17. On December 22,

1996, a downpower to 96 percent and later to 90 percent was conducted in order

to recover from a feedwater heater transient and to reseat a relief valve that

lifted on the 5B Feedwater Heater. The 5B Feedwater Heater relief valve

lifted while attempting to place the 6A Feedwater Heater level control

instrument in service following an air-line failure to the level controller.

I. Operations

01

Conduct of Operations

01.1 General Comments (71707)

The inspectors conducted frequent control room tours to verify proper

staffing, operator attentiveness and communications, and adherence to

approved procedures. The inspectors attended operations turnover, and

management review meetings to maintain awareness of overall plant

operations. Operator logs were reviewed to verify operational safety

and compliance with Technical Specifications (TSs). Instrumentation,

computer indications, and safety system lineups were periodically

reviewed from the Control Room to assess operability. Plant tours were

conducted to observe equipment status and housekeeping. Condition

Reports (CRs) were reviewed to assure that potential safety concerns and

equipment problems were reported and resolved. Specific events and

noteworthy observations are detailed in the sections below.

01.2 "C"

Auxiliary Boiler Water Hammer Incident

a. Inspection Scope (71707)

On December 20, while placing the "C"

Auxiliary Boiler in service, a

water hammer occurred downstream of the boiler in the piping to the C

Auxiliary Boiler Deaerator Tank. The inspectors reviewed the

circumstances leading to the water hammer, discussed the incident with

engineering personnel who were investigating the incident, and walked

down the piping to determine if all damage was properly identified by

the licensee.

b. Observations and Findings

On December 20, operations personnel were placing the "C"

Auxiliary

Boiler in service in accordance with Operations Procedure (OP)-401,

Auxiliary Heating Steam, Rev. 31. The purpose for starting the "C"

Auxiliary Boiler was to supply supplemental heating steam to certain

areas of the Auxiliary Building due to decreasing outside environment

temperatures. When valve AS-2317, the Auxiliary Steam to the "C"

Auxiliary Boiler Deaerator Tank', was opened in accordance-with the

procedure, evidence of a water hammer was heard downstream of AS-2317 in

2

the piping to the C Auxiliary Boiler Deaerator Tank. Boiler startup was

suspended and engineering personnel were notified of the incident and

requested to inspect the affected piping for any damage. Although no

damage was identified as a result of the incident, an investigation was

initiated to determine the root cause of the water hammer.

The licensee determined that the water hammer was the result of a drain

valve lineup problem associated with OP-401. The procedure required

that AS-2317 be closed whenever the C Auxiliary Boiler was not in

service. Closing AS-2317 also isolated a downstream steam trap allowing

steam trapped in the piping to condense and form voids in the piping.

When AS-2317 was opened during startup of the boiler, the sudden re

pressurization of the piping resulted in a water hammer.

The licensee planned to revise OP-401 to ensure that AS-2317 remained

open and provisions for verifying that the piping downstream of AS-2317

was properly drained of condensation prior to placing the C Auxiliary

Boiler in service. An operations clearance was placed on the C

Auxiliary Boiler until the procedure was revised. The inspectors

conducted a walkdown of the affected piping following the event. No

damage to the affected piping was observed from this walkdown.

At the end of the inspection period, the licensee was still

investigating the reason why OP-401 had been written to allow the

improper lineup that allowed the potential for a water hammer event. A

procedure discrepancy was evident since plant piping details showed the

normal lineup for AS-2317 as open. The results of the licensee's

investigation and associated corrective actions to address the procedure

problem were to be documented in CR 96-03184, which was initiated to

address this incident.

The inspectors noted that this was the third steam or water related

hydraulic transient that had occurred over the past several months. For

example, in September 1996, during plant shutdown for refueling outage

17, a water hammer was introduced in certain feedwater heater drain

lines as a result of re-admitting steam to the Moisture Separator

Reheaters which had previously been isolated during plant cooldown. In

October, during reactor coolant system check valve leakage testing, a

water hammer occurred in the Safety Injection cold leg injection piping

as a result of not adequately re-pressurizing the piping during testing

restoration. In both of these two incidents, the primary cause was the

result of inadequate procedures controlling the system or test

alignment. In each of the three incidents, the problems associated with

the procedures had gone uncorrected over many years even though the

procedures had been used periodically. The inspectors noted that this

indicated a lack of sensitivity to recognizing and resolving minor

hydraulic transient problems.

The inspectors have noted a heightened awareness by operations and

engineering personnel/management to the potential for hydraulic

transients since the first two incidents discussed above. The

3

identification and detailed investigation of the C Auxiliary Boiler

water hammer transient was an example of this heightened awareness.

The licensee indicated that a more detailed review of all operations

system lineup and test procedures would be conducted to ensure that

other configuration problems which could lead to potential hydraulic

transients were identified and corrected.

c. Conclusions

The inspectors concluded that operations personnel demonstrated a

heightened sensitivity to potential hydraulic transients with the

identification of this incident. Engineering performed a detailed

investigation of the transient and were successful in identifying the

root cause. The licensee's planned corrective actions were appropriate

to address the procedure discrepancy identified, as well as the generic

implications of other potential procedural configuration weaknesses.

While the Auxiliary Boiler is not a safety related system, the

inspectors noted that continued licensee emphasis and sensitivity to

potential hydraulic transients was warranted due to past weaknesses in

this area.

01.3 Crack in the Emergency Diesel Generator Room Roof

a. Inspection Scope (37551, 71707)

The inspectors reviewed and discussed with the licensee, CR 96-03202

that was generated due to a noted crack in the concrete roof of the B

Emergency Diesel Generator (EDG) building.

b. Observations and Findings

The condition report was originated when an operator noted some water

dripping from the roof into the EDG room. Upon noticing the condition,

Robinson Engineering Support Section (RESS) was notified. Further it

was verified that no water was dripping onto electrical equipment within

the EDG room. The inspectors performed a walkdown of the EDG building,

including the roof with the licensee and discussed the condition with

the assigned structural engineer. The crack was not obviously visible

from the EDG room.

An evaluation associated with the condition report concluded that the

seismic/structural integrity of the building was not negatively impacted

by the crack in the EDG roof and that the ability to maintain negative

pressure in the auxiliary building was maintained. As immediate

corrective action, the affected area of the roof was re-coated with a

sealing paint. Additionally, the licensee plans to re-coat the entire

roof with a flexible water tight sealing material. Action request (AR

96-05410) was initiated by the licensee to track this planned corrective

action. The inspectors plan to continue to periodically monitor this

issue during the conduct of routine inspections.

c. Conclusions

The inspectors concluded that the operator acted appropriately upon

noting the abnormal condition relative to water dripping into the EDG

room. Further, the crack did not impact the operability of the EDG.

01.4 Failed Instrument Air Line Affecting 6A Feedwater Heater

a. Inspection Scope (71707, 62707, 37551, 40500)

An Instrument Air (IA)

line associated with a feedwater heater level

controller failed initiating a minor transient as well as power

reductions. The inspectors assessed licensee activities associated with

the event. CRs 96-03194 and 96-03195 were generated as a result of the

event.

b. Observations and Findings

On December 22, 1996, while Robinson Unit 2 was at 100% power, an

instrument air line on the 6A Feedwater Heater level controller (LC)

failed such that the 6A Feedwater Heater level control valves (LCV)

1508A and 1508B failed closed. With the 6A Feedwater LCVs closed, the

drain path to the heater drain tank was isolated and the 6A Feedwater

Heater shell side level started to increase. This initiated a transient

which manifested in a level deviation in the C Steam Generator (S/G) due

to lower S/G level and an increase in power to approximately 101.4 %.

The control room responded to the level deviation alarm and reduced

power to approximately 96%. Following restoration of S/G level and

stabilization of the transient, the plant was returned to full power.

The 6A Feedwater heater alternate LCV 1508B was opened to allow shell

side blow-through.

Troubleshooting and repairs were performed and the failed section of the

copper instrument air tubing to the LC was replaced. A small crack was

noted in the IA line which was attributed to cycling of the tubing for

connection and disconnection purposes. Upon discussion, the inspectors

were informed that the plant had experienced other problems with the IA

system, and consequently, the IA system is being carried as a "TOP 10"

item to appropriately prioritized attention and resources. The failed

portion of the IA tubing was replaced.

Additionally, since the 6A Feedwater Heater High level alarm had not

come in as expected following the closure of the LCVs, the shell side

level switch was checked and demonstrated to operate properly.

During the restoration to normal alignment following repairs, the SB

Feedwater Heater shell side relief valve HDV-381B lifted. Consequently,

a power reduction was initiated and the relief valve reseated at

approximately 90%. The restoration was being performed at full power

and it.involved transferring the 6A Feedwater Heater level controls from

the alternate to the primary LCV (i.e. from LCV 1508B to LCV 1508A).

The licensee is postulating that during this transfer, a pressure

5

perturbation occurred and was transmitted through the heater drain tank

to the 5B Feedwater Heater. The inspectors questioned whether the

licensee decision to restore the 6A Feedwater Heater to normal alignment

at full power was conservative. The licensee plans to review this

issue, including assistance from RESS, through the condition report

process.

Initially, the licensee believed that the relief valve had prematurely

lifted at approximately 176 psig with an expected setpoint of 225 psig.

This was based on the system pressure readings as observed on Emergency

Response Facility Information System (ERFIS) reading approximately 176

psig. However, upon further review, the licensee believes that the

system pressure did probably reach 225 psig and the data sampling

frequency of ERFIS was such that it did not capture the instantaneous

system pressure that caused the relief valve to lift.

Feedwater heater relief valves, including HDV-381B are not periodically

tested. Consequently, a work request was initiated to test the relief

valves on the 3A, 3B, 4A, 4B, 5A, 5B, 6A, and 6B heaters during the next

scheduled outage. Further, the licensee will assess the periodic

testing of the relief valves through the condition report. Upon

questioning, the inspectors were informed that the lifted relief valve

setpoint, if changed due to the lifting, is more likely to have lowered.

c. Conclusions

The inspectors concluded that a reliability problem associated with a

portion of the IA system resulted in a transient on the secondary side.

Continued licensee attention to address this issue, as well as periodic

testing of-secondary relief valves is warranted. The decision to

restore the 6A Feedwater Heater to normal alignment at full power was

considered a weakness.

07

Quality Assurance In Operations

07.1 Plant Nuclear Safety Committee Meeting

a. Inspection Scope (40500)

The inspectors evaluated certain activities of the Plant Nuclear Safety

Committee (PNSC) to determine whether the onsite review functions were

conducted in accordance with TS and other regulatory requirements.

b. Observations and Findings

On December 18, 1996, the inspectors attended the PNSC meeting during

which the committee reviewed an evaluation of SOER 96-1, Control Room

Supervision, Operational Decision Making, and Teamwork; a violation

response and procedural revisions; and a presentation from the Nuclear

Fuels Group on the disposition of the error in the Siemens' code for a

large break loss of coolant accident (LBLOCA). The presentations were

thorough and the presenters readily responded to all questions. The

  • 6

committee members asked probing questions and were well prepared. The

committee members displayed understanding of the issues and potential

risks. The inspectors considered that the chairman appropriately

limited discussion to the issues and their safety ramifications.

c. Conclusions

The inspectors concluded that the onsite review functions of the PNSC

were conducted in accordance with TSs. The PNSC meeting attended by the

inspectors was well coordinated and meeting topics were thoroughly

discussed and evaluated.

07.2 Effectiveness of Licensee Controls in Identifying, Resolving, and

Preventing Problems

The licensee has provided a site-wide, common program for identifying

issues that require corrective action. The goal of the program was to

improve overall plant performance by correcting conditions adverse to

quality. During this inspection, the inspectors reviewed the

administrative and procedural aspects of the program, the effectiveness

of the corrective actions, the self-assessments and audits of the

program, and other processes that provided for the incorporation of

operating experience feedback.

1.

Corrective Action Program

Inspection Scope (40500)

The licensee's procedure, PLP-026, Corrective Action Program, Rev. 24,

was reviewed by the inspectors. In addition many of the specific

elements of the program and completed CRs were reviewed.

Observations and Findings

The inspectors reviewed 7 CRs which were classified as significant CRs

in accordance with PLP-026. The inspectors verified that operability

assessments were performed, management reviews were completed,

evaluations and recommended corrective actions were appropriate, and

when required, appropriate immediate corrective actions were performed

based on the nature of the problem. The following CRs were reviewed by

the inspectors and determined to be appropriately dispositioned.

95-01873: Inadequate corrective actions to respond to NAS

findings,

96-02272: Position of Containment butterfly valves,

96-02471: Cutting of incorrect conduit during plant

modification,

96-02754: Water hammer during safety injection accumulator

piping surveillance test,

95-01523: Inadvertent Residual Heat Removal pump start,

95-02216 - Unexpected Emergency Diesel Generator start during

clearance tagout, and,

95-01661 - Main Feedwater Isolation following high Steam Generator

level.

In addition to assessing the program, the inspectors reviewed another

sample of Condition Reports. Within the sample it was found that about

20% had been deferred to provide an extension of time for corrective

action, and about 44% required more time for evaluation.

Deferrals are permitted by PLP-026, with restrictions. The restrictions

include specific level of management approval for the first two

extensions. If an additional extension is needed, approval from the

Site Vice-President is required. The deferral rate was acceptable. The

inspectors concluded that the controls in place have kept the number of

CR deferrals in check. The inspectors did not find any deferred CRs

without a valid reason, nor did the deferral have an adverse effect on

safe plant operations. This.area was reviewed for trends by the Self

Assessment Manager to assure that items were not improperly deferred.

The inspectors screened 107 CRs that were voided in 1996 and observed

that 40% were duplicates or were incorporated into another CR.

Approximately 25% contained insufficient data to verify that CR voiding

was appropriate, including 2 CRs which had no entry in the reason for

voidance field. Based on further discussion and review of the reason

for voidance, the dispositioning of the sample of voided CRs reviewed

was acceptable.

Other CRs were voided and the reason stated for voidance on the form

indicated that the item would be resolved by another mechanism.

However, in some cases the issue was not resolved. Paragraph 5.1.2.1 of

PLP-026 addresses the method to void CRs which, after evaluation, are

determined to not meet the definition of an adverse condition. The

procedure indicates that the reason for voiding a CR is to be documented

on a CR change form. The inspectors reviewed eleven randomly selected

"voided" CRs to verify the concerns documented on the CRs did not

constitute an adverse condition, and that voiding of the CR was

appropriate. The voided CRs reviewed were 96-00349, 96-00502, 96-00543,

96-01094, 96-02765, 96-00391, 96-00566, 96-00601, 96-00893, 96-02195,

and 96-01356. The inspectors concluded that none of the concerns

documented on the "voided" CRs met the definition of an adverse

condition. However, review of the "voided" CR resolutions disclosed

that the reason the CRs were voided was not always well documented.

Examples identified were as follows:

CR 96-00349 involved a procedure which required re

verification of the containment equipment hatch opening

times each time the hatch is opened. The reason for voiding

8

stated that the CR was intended to be an engineering service

request (ESR).

The inspectors determined that an ESR was

initiated (number 96-0122) but was later deleted since the

existing procedure was determined to be appropriate. The

inspectors did not identify a problem with the resolution of

the issue although the final disposition was not well

documented in the CR.

CR 96-00502 involved an error found on one of the original

plant construction drawings. The reason for voiding

documented on the CR stated that a drawing change request

(DCR) was initiated to revise the drawing. The inspectors

determined that a DCR (number 96-168) was issued, but later

also was voided. The final disposition of this concern was

to delete the drawing since it was no longer required.

However, this was not documented in the CR.

CR 96-00543 concerned a potential incorrect fire barrier

(penetration) design. The reason for voiding stated on the

CR was that engineering felt that this issue had been

previously evaluated, but that if the documentation could

not be provided, a new CR would be issued. Discussions with

the engineers involved in the resolution of the issue

disclosed that the concern had been evaluated, as stated on

the CR, and that the as-built design was acceptable.

However, a reference to the final disposition of the issue

was not documented in the CR.

CR 96-01094 concerned an equipment item which had not been

installed. An ESR, number 96-00272, was issued to resolve

the issue. The CR was voided pending resolution of the ESR.

The inspectors determined that ESR 9600272 was deleted by

ESR 9600476 which was still open. The final disposition of

the concern was not documented on the CR.

CR 96-02765 concerned an error on a safety-related system

flow diagram. The reason for voiding the CR stated that a

DCR would be issued to correct the problem. The inspectors

determined that DCR 96-1103 was issued to correct the

drawing and that the DCR (drawing correction) was being

implemented.

CR 96-00391 involved a potential inadequate review of significant

event report 92-012 regarding potential reverse rotation of

containment fan units when in standby or shutoff. The reason for

voiding the CR was not documented. Theinspectors reviewed the CR

resolution with licensee technical support and operations

personnel and determined that procedural controls were utilized to

prevent this problem as well as monthly surveillance. The

resolution was acceptable although the disposition was not

documented in the CR.

9

CR 96-00601 involved a potential spread of contamination issue

regarding High Efficiency Particulate Air (HEPA) filter hose left

open. Procedural requirements include sealing the hose after use.

It was later determined that the unit was still in use and did not

require sealing at that time. The inspectors determined that the

resolution was acceptable but the disposition was not documented

in the CR.

The inspectors also reviewed three additional "voided" CRs and concluded

that the reason for voidance was clearly documented in the CR. These

were CR numbers 96-01091, -01402, and -01941.

The inspectors identified the following as a weakness in the licensee's

corrective action program:

Incomplete/improper documentation of the

reasons for voiding a CR, and/or voiding a CR based on some planned

action when the action was still incomplete when the CR was voided.

Significant CRs are required to be evaluated within 14 days and

completed within 60 days of the evaluation approval date. Extensions or

deferrals are periodically reviewed for adverse trends by the management

of the Self-Assessment Section. Program data showed that about 2500 CRs

are initiated per year and that all organizations were actively involved

in the program. Corrective Action Program (CAP) tracking and data

trending was good and the backlog was under control. The program

recognition "Catch of the week" provided positive incentives. The

Operating Events Assessment unit involvement provided program oversight

which contributed to the success of the program. Management and site

personnel had a positive attitude toward the program.

Section 5.13.1.2 of PLP-026 requires each site section or unit to

perform a quarterly analysis of CR data to detect trends. The

inspectors reviewed the analysis of the trends based on condition

reports performed for the third quarter of 1996 in the Robinson

Engineering Support Section, maintenance, and operations units. The

analysis of the CR data indicated some potential adverse trends which

the managers in the units documented on new CRs to evaluate and develop

corrective actions to resolve the issues. The inspectors also attended

a weekly Robinson Engineering Support Section managers meeting during

which CRs identified during the previous week were discussed by the unit

managers to address corrective actions, causes of the CRs. and steps to

take to avoid similar CRs.

The OEA Manager performed trending and evaluation of the CR process.

The data indicated that the CR backlog was not trending up and CR

tracking was adequate for program control. The inspectors concluded

that the trending of CR data by unit managers was an effective method to

identify and reverse problems and adverse trends, and improve-overall

plant performance.

A sample of about 3000 CRs was examined to determine which

organizational component was identifying the issues and who was fixing

them. The following results were found:

Organizational Component

% Found

% Fixed

Environ. & Radiation Control

24

20

Operations

14

10

Maintenance

11

15

Mechanical Systems

9

14

Nuclear Assurance Section

8

8

Security

7

6

Outage & Scheduling

6

6

Elec I&C

4

9

Others

17.

20

From the above data, it was evident that all organizational components

were finding and fixing problems within their area. In some cases, such

as maintenance and operations, CRs that were identified by their own

personnel were assigned to another organizational component for

corrective action. This was expected.

Several managers directly involved within the licensee's problem

identification process and corrective action program were interviewed to

determine the extent of their understanding of the process and their

feelings toward ownership of the program. Those selected were from

maintenance, engineering, plant support, operations, and quality

assurance. The subjects discussed at these interviews included: the

extent of their involvement, amount of resources devoted to the program,

and, how well they thought the program was working.

All personnel interviewed accepted the program and were using it as

intended. It was evident to the inspectors that significant resources

were devoted to this program.

The inspectors reviewed the audits of the CAP conducted by NAS and

Performance Evaluation Section, and the reviews of the Corrective Action

Program by the onsite and offsite review committees. Self-assessments

reports were also reviewed. The findings and actions taken by the

various audits and reviews were examined for timeliness and

completeness.

Additional areas of the CAP were reviewed as follows:

a sample of recent events and issues were reviewed to determine

if a CR was prepared for the item,

the weekly Operating Experience Assessment Unit Weekly staff

meeting and a Failure Prevention Inc. Users Group meeting were

attended by the inspectors, and,

a sample of significant, completed, and voided CRs were reviewed.

Conclusions

Based on review of selected CRs, the inspectors concluded that the

licensee's corrective action management program was implemented in

accordance with PLP-026 and UFSAR Section 17.3, Robinson Quality

Assurance Program Description.

In general, all organizational components were finding and fixing

problems within their area. CRs were discussed on a regular basis, at

least weekly, and were assigned for action. CR assessments were

thorough and root cause analyses were good. Trending of CR data by unit

managers was an effective method to identify and reverse problems and

adverse trends, and improve overall plant performance.

Several potential adverse conditions were voided with poor

documentation. A need for training was indicated by the number of

voided CRs with poor documentation. The large number of voided CRs

indicated a weakness in personnel awareness of what constituted an

adverse condition.

Self-assessments in Engineering, and Materials and Contract services

indicated a need for training. NAS assessment 96-01 identified a

weakness in the understanding of the CR process. Discussions with plant

personnel disclosed that there was no formal training provided to

personnel, other than CR evaluation personnel.

2.

Operating Experience Program

Inspection Scope (40500)

The inspectors reviewed the licensee's Operating Experience (OE)

Program.

Observations and Findings

Operating Experience is a part of the overall H. B. Robinson CP&L

quality assurance process. The Operating Experience program ensures

industry data is sent to applicable Robinson work units and that

Robinson specific experience and data is supplied to other CP&L sites

and the nuclear industry as appropriate. The inspectors reviewed

Robinson procedure PLP-107, Operating Experience Program, Revision 0,

dated June 26, 1996. This procedure provided the requirements for

establishing the Robinson Operating Experience program including source

document receipt, screening, evaluation, recommended actions, action

tracking, action closeout and program status reporting.

OE feedback item applicability screenings, OE item evaluations, OE unit

self-assessments, OE program Nuclear Assurance Section (NAS) audits, and

OE tracking and work backlogs were reviewed. The inspectors attended

the weekly Operating Experience Assessment (OEA) meeting, interviewed

plant personnel and observed end use activities of the OE program.

12

OE source document screening items 5751, 5761, and 5774 were reviewed.

The screening reviews were performed in accordance with PLP-107 and the

applicability review and recommended actions were acceptable. The

inspectors reviewed completed OE item evaluations 96-00636, 96-00955,

and 96-01923. The evaluations were completed in accordance with PLP-107

and were thorough.

Self-assessments and NAS audits were performed on the OE program. The

inspectors reviewed OE self-assessments: 0EA 96-05, SOER/OSU 96-03,

SOER/0EF 96-02, OEA 96-01 and R-OE-95-01. NAS audits RSOER 96-01 and R

CA-96-01 were reviewed. Both the NAS audits and OE self-assessments

identified that procedures did not incorporate Significant Operating

Experience Report (SOER) references. CR 96-00956 was initiated for

resolution of this item. The inspectors concluded that the self

assessments and NAS audits were thorough and that the findings were

substantive. The licensee was taking actions to address the findings.

The inspectors attended the OEA unit weekly status meeting and observed

that the staff reviewed the OE items screened for the week and verified

the acceptability of the item dispositioned. Condition Reports

processed for the week were also reviewed including the CR

classification. The OEA staff selected one corrective action/

improvement item identified each week and provided an award and mention

for the CR initiator in a licensee newsletter. This provided positive

feedback for the problem identification process and demonstrated

commitment to problem self identification and resolution.

The OEA unit tracking and work backlog was reviewed. A monthly report

was prepared by the OE reviewer which addressed the items processed for

the month and tracked the evaluations issued, and the status and age of

open evaluations. The OE backlog was examined and the inspectors

determined that the backlog was not excessive and no evidence was noted

of items being deleted or deferred.

The licensee had incorporated OE feedback data into several routine

activities. The inspectors observed that OE feedback items were

discussed at morning shift turnover meetings. The checklist for

conducting pre/post job briefings requires that the briefing include a

discussion of applicable OE data for the evolution. An OE item file by

system was maintained in the control room for use in conjunction with

the OE database for conducting briefings. The files contained

experience data identified by the NRC, INPO, and other CP&L sites. The

frequent use of OE data in routine daily activities was viewed as a

strength.

Discussions with site personnel indicated that performance during the

outage was improved with the emphasis on frequent use of CE data. OE

information was used in briefings for all the major evolutions of

shutdown, cooldown, startup, and heatup. The recent safety injection

system water hammer event was an example where previous experience did

not preclude a similar event.

13

Conclusions

The Operating Experience Program was determined to be effective. The

completed OE evaluations reviewed were acceptable. The OE self

assessments and NAS.OE audits were thorough. The OEA weekly status

meeting, monthly report, and OE tracking provided good program

oversight. The incorporation of OE data into routine daily activities

was viewed as a strength.

3.

Self-Assessment Activities

Inspection Scope (40500)

The inspectors reviewed self-assessment activities performed within the

Robinson line organizations.

Observations and Findings

Self-assessments are part of the overall CP&L quality assurance program

at Robinson. Self-assessments are critical evaluations of activities,

processes, or programs performed by the individuals or organizations

accountable for the work. The results of these assessments are

categorized as strengths, or findings. Findings may be adverse

conditions, areas not meeting expectations, or areas needing

improvement. The inspectors reviewed Robinson procedure PLP-057, Self

Assessment, Revision 5, dated September 16, 1996. This procedure

specifies the requirements for establishing the self-assessment program

including development of an annual self-assessment plan, the frequency

for self-assessments, areas to be covered, e. g., the corrective action

program in each work unit, conducting assessments, reporting results,

and follow-up activities.

The inspectors reviewed the 1996 Self-Assessment plans for the following

Robinson work units: the engineering support section, training,

operations, maintenance, materials and contract services, and the

Robinson NAS. The inspectors noted that the majority of the planned

assessments were performed on schedule, assessments were not being

canceled or deleted, and assessments were added to the schedule or were

being rescheduled (planned dates moved-up) to respond to events which

occurred at other sites. The licensee also performed additional

assessments if findings were identified which appeared to have generic

implications. An example of this was the self-assessment of the 50.59

process in the Robinson Engineering Support Section which indicated

deficiencies in the quality and documentation of safety evaluations

performed for design changes. A site wide assessment was performed by

NAS to determine if similar problems existed in 50.59 evaluations

performed by other site work units. The inspectors also noted that

assistance was provided by personnel from other sites and other

organizations to perform some of the self-assessments. The use of

individuals from other organizations provides additional insight in the

various processes which are being evaluated. The self-assessments

covered all major functional areas.

14

The inspectors reviewed the following self-assessments:

R-96-OP-04: Operator Actions not Covered by Procedures,

MNT 96-01: Effectiveness of Maintenance CAP Program,

MNT 96-05 - UFSAR Commitments,

TRAIN 96-03 - Training Section Corrective Action Program,

RESS 96-09 - RESS Corrective Action Program,

RESS 96-12 - Temporary Modification Control (follow-up),

RESS 96-15 - RESS Organization & Administration,

RESS 96-18 - Engineering Product Quality,

RESS 96-26 - Environmental Qualification,

RESS 96-31 - Identification and Updating of Affected Design

Documents (follow-up),

RESS 96-32 - Safety Review Screening,

RAS 96-01 - 10 CFR 50.59 Program, and,

M&CS/P 96-06 - Corrective Action Program.

From review of the above self-assessments, the inspectors determined

that CRs were initiated when findings in self-assessments were

identified as adverse conditions, follow-up reviews were performed, and

improvement CRs were initiated to track recommended actions resulting

from self-assessments. Licensee management was actively involved in

monitoring the results of the self-assessments and monitoring the

overall effectiveness of the program.

Conclusions

The inspectors concluded that the self-assessment program at Robinson

has been effective in identifying performance deficiencies and was

useful in providing oversight to management. Managers have been

proactive in following up on issues identified at other sites to

identify and correct deficiencies at Robinson. The inspectors also

concluded that licensee management was committed to the self-assessment

process as indicated by the resources, including assistance of outside

organizations, involved in the self-assessment process, and the number

of self-assessments performed on an annual basis.

15

08

Miscellaneous Operational Issues (92901)

08.1

(Closed) VIO 50-261/95-21-01, Operator Failure To Monitor Plant Status:

This violation was issued because operators failed to adequately monitor

steam generator (S/G) levels and take appropriate actions. As a result,

a high S/G level trip occurred. The root causes were determined to be

personnel error (inattention to detail and misjudgment) by operations

personnel, and equipment degradation of feedwater regulating valves

(FRVs) and FRV bypass valves. The corrective actions included event

review with operating crews, additional emphasis on operations self

assessments, improvement to pre-job and post-job briefings, evaluation

of FRV bypass valve leakage, and revisions to operator event simulator

training. The inspectors reviewed shift personnel statements, event

review training records, Operations Shift Error Prevention Plans,

discussed pre-job and post-job briefing changes with operations

personnel, Engineering Evaluation of FRV bypass valves leakage, Training

Scenario EPP-4 Reactor Trip Response, and scenario training records.

The inspector verified the corrective actions described in the

licensee's response letter, dated September 11, 1995, to be reasonable

and complete. The corrective actions addressed the event root cause.

Two new corrective actions subtasks were established to implement FRV

bypass valve vendor recommendation for improving valve leakage

performance at the next valve overhaul. This item is closed.

08.2 (Closed) VIO 50-261/95-27-01, Inadequate Clearance Results In

Unexpected Emergency Diesel Start: This violation was issued because an

unexpected Emergency Diesel Generator (EDG) start occurred while

implementing a clearance for scheduled maintenance. An inadequate

clearance boundary allowed air trapped in the air start piping to start

the engine. An incorrect assumption was made that the volume of trapped

air would not start the engine. The licensee and vendor evaluated the

event and determined that no engine damage occurred. This EDG

evaluation was described in NRC Inspection Report 50-261/95-27 as

adequate. The event cause was due to personnel error. The corrective

action included performing the evaluation of the EDG and providing

training. The inspectors reviewed the EDG evaluation (ESRs 9500990 and

9500993), the work request which inspected the EDG (WR/JO 95ALTZ1), and

the records for the training on venting/draining requirements and the

need for conservative decisions regarding operation and clearances for

Engineered Safety Features equipment of procedure Operations Management

Manual (OMM)-005, Clearance and Test Request. The inspectors verified

the corrective actions described in the licensee's response letter,

dated December 14, 1995, to be reasonable and complete. The corrective

actions addressed the event root cause. This item is closed.

08.3 (Closed) VIO 50-261/96-01-01, Auxiliary Feedwater System Valve

Misalignment: On January 16, 1996, during a walkdown of the accessible

areas of the Auxiliary Feedwater (AFW) System, the inspectors identified

that two valves were not in the specified position. Operating Procedure

(OP)-402, Auxiliary Feedwater System, Revision 38, Attachment 9.1, AFW

Valve Checklist requires that valves AFW-110 and AFW-111 be in the full

open position. The inspectors observed that these valves were in the

16

throttled position and notified the Shift Supervisor. An auxiliary

operator(AO) later verified that the valves were 60% open and placed

them in the specified position. CR 96-00126 was initiated to follow

this item.

The licensee performed an extensive investigation and concluded that the

most probable cause for AFW-110 and AFW-111 to be found 60% open was

flow induced vibration. Testing would not have detected the

mispositioned valves. The valves are in the recirculation line of each

motor driven AFW pump and allowed sufficient flow to meet the

surveillance acceptance criteria.

On February 13, 1996, during the performance of Operations Surveillance

Test (OST)-201-B, MDAFW System Component Test-Train B (Monthly), the AO

who was performing the test and a system engineer who was assisting

observed that AFW-111 vibrated five full turns in the closed direction.

CR 96-00359 was initiated to follow this issue. The licensee's

corrective action was to lock open valves AFW-110 and AFW-111 and revise

the flow diagram. CR 96-00126 was also revised to reflect the CR 96

00359 corrective actions. Additional corrective actions were to revise

Operations Management Manual (OMM)-001, Conduct of Operations, to

provide additional guidance for valve verification. PLP-030,

Independent Verification, was also revised to reflect the changes of

OMM-001. The event was reviewed with the operators during training.

The inspectors reviewed Flow Diagram G-190197, Revision 38, Sheet 4 and

verified that valves AFW-110 and AFW-111 were locked open. They

reviewed lesson plans and training records and verified that training

was given to the operators. The corrective actions have been completed

and this item is closed.

II. Maintenance

M1

Conduct of Maintenance

M1.1 General Comments

a. Inspection Scope (61726 and 62707)

The inspectors observed all or portions of the following maintenance

related WRs/JOs and surveillances and reviewed the associated

documentation:

WR/JO 95-ANLEl: Replacement of Instrument Air Check Valve IA-474

WR/JO 96-AIPP-003: "B" Instrument Air Compressor Preventative

Maintenance

WR/JO AHVN-001: Thermal Overload Testing of 480V Breaker for

Motor-Operated Valve CC-749A

17

OST 352-2: Containment Spray Component Test - Train B, Rev. 2

b. Observations and Findings

The inspectors observed that these activities were performed by

personnel who were experienced and knowledgeable of their assigned

tasks. Work and surveillance procedures were present at the work

location and being adhered to. Procedures provided sufficient detail

and guidance for the intended activities. Activities were properly

authorized and coordinated with operations prior to start. Test

equipment in use was calibrated, procedure prerequisites were met,

system restoration was completed, and surveillance acceptance criteria

were met.

c. Conclusions

The inspectors concluded that maintenance and surveillance activities

were performed satisfactorily.

M1.2 Lack of Comprehensive Preventive Maintenance for Freeze Protection

Circuits

a. Inspection Scope (62707)

The inspectors continued folTowup on several maintenance related issues

identified during the previous inspection report period involving Freeze

Protection (FP) circuitry. Additionally, the inspectors reviewed the

licensee'As evaluation of an anomaly in the output of the Steam Generator

and Steam Header pressure transmitters due to a FP circuitry failures.

b. Observations and Findings

During the previous inspection period, the inspectors conducted a review

of the licensee's cold weather protection program. Associated with this

review, the inspectors performed a walkdown of the selected FP circuitry

status panels and identified that several FP circuit status lights were

not illuminated when they should have been. Also, the inspectors noted

that the settings for FP circuitry thermostats were not periodically

verified to be at their proper setpoint to ensure that the circuits

energized and deenergized at the proper temperature. Based on

discussions with the Electrical/Instrumentation & Control (I&C)

supervisor during the earlier inspection, the licensee felt that other

surveillances being performed by either I&C or operations would identify

any circuitry problems. These other surveillances included the periodic

manual energization of FP circuits and measurement of the current drawn,

and operations personnel requirement to monitor for FP circuit status

lights that were not illuminated.

During this report period, the inspectors verified that appropriate

repairs were performed to correct the problems previously identified

with the FP circuits.

18

Also during this report period, the licensee identified an example where

a FP cabinet heater thermostat for the Steam Generator pressure

transmitters failed to deenergize which caused excessive cabinet

temperatures. This resulted in the output of the transmitters

indicating higher than actual pressures. This problem was identified by

operations personnel on December 12, 1996, when it was noticed that

whenever the FP cabinet heater energized, an increase in steam pressure

occurred. The worst case observed was approximately 10 psig. This

problem was significant since the output of the steam pressure

transmitters provide inputs to the reactor protection system.

The

higher pressure signals could result in exceeding the analyzed values

for the instrument uncertainties. A similar problem was identified when

the FP circuitry in the Steam Header pressure transmitter cabinets. Due

to one of the heaters in this cabinet being miswired, it remained

energized all the time, resulting in higher than expected temperatures

inside.

The inspectors reviewed CR 96-03075 which documented these incident.

The results of an engineering evaluation on the effect of the increase

in steam generator and steam header pressure outputs determined that the

available margin in the instrument uncertainty calculations was not

exceeded. The licensee's corrective actions for these problems included

a review of all transmitters subject to freezing for proper freeze

protection design and the addition of periodic preventive maintenance

for checking the operability and setpoint of FP thermostats. The

inspectors determined that the licensee had adequately evaluated and

proposed adequate corrective actions to address this issue.

c. Conclusions

The inspectors concluded that the lack of comprehensive preventive

maintenance on Freeze Protection circuitry was a weakness in the

licensee's cold weather protection program. Had there been preventative

maintenance to verify the operability of Freeze Protection thermostats,

the problems associated with the thermostats in the Steam Generator and

Steam Header pressure transmitter cabinets could have been identified

previously.

Operations personnel identification and response to the anomaly between

Steam Pressure transmitter output and energization of Freeze Protection

circuitry was considered an example of good attention to detail and

plant monitoring.

Engineering thoroughly evaluated Steam Generator and Steam Header

pressure transmitter output anomalies that were caused from higher than

design cabinet temperatures resulting from Freeze Protection system

malfunctions.

M8

Miscellaneous Maintenance Issues (92902)

.

M8.1 (Closed) VIO 50-261/95-19-05, RHR Pump Start Due to Troubleshooting:

This violation was issued because adequate measures were not established

19

to prevent inadvertent operation of B RHR Pump during troubleshooting of

a defective relay. The licensee's root cause evaluation determined

personnel error as the cause of the event. No positive controls were

used to prevent inadvertent pump start. The event was reviewed with

shift operations personnel and maintenance mechanics and technicians.

The inspectors reviewed the records of this training and verified that

Procedure Maintenance Management Manual MMM-001, revision 29 contained

the requirement that maintenance personnel will use positive controls

such as clearances, caution tags or procedural guidance to prevent

inadvertent equipment operation. The inspectors verified the corrective

actions described in the licensee's response letter dated August 23,

1995, to be reasonable and complete. The corrective action addressed

the event root cause. This item is closed.

M8.2 (Closed) LER 50-261/95-06-00, Technical Specifications Violation Due To

Failure To Meet Minimum Degree Of Redundancy:

and,

(Closed) LER 50-261/95-07-00, Condition Prohibited By Technical

Specifications Due To Failure To Meet Minimum Degree Of Redundancy:

and,

(Closed) LER 50-261/95-07-01, Condition Prohibited By Technical

Specifications Due To Failure To Meet Minimum Degree Of Redundancy:

and,

(Closed) LER 50-261/95-08-00, Condition Prohibited By Technical

Specifications Due To Failure To Meet Minimum Degree Of Redundancy:

On September 3, October 29, and November 5 and 14, 1995, the licensee

had similar events. The first three events were caused by the

Overtemperature Delta-Temperature (OTDT) Temperature Indicator and the

fourth was caused by the Overpower Delta-Temperature (OPDT) setpoint

indicator drifting beyond their acceptable tolerances and the associated

protection channel was declared inoperable. The minimum degree of

redundancy as required by Technical Specification 3.5, Table 3.5-2,

Items 5 and 6 could not be satisfied until the channel was placed in a

tripped condition. These event are described in detail in the subject

LERs.

CRs 95-02062, 95-02556, 95-02618, and 95-02687 were issued to track each

of the events. The licensee combined the November 5 and October 29

events into a single LER (95-07) as the second event was caused by an

improper installation of a component. Hardware inspection revealed that

a failed capacitor was the cause of the OTDT drifting. The licensee

determined that the electrolytic capacitors in the Hagan modules would

be replaced. A Technical Specification change to provide an allowed

outage time for instrumentation channels was one of the proposed

corrective actions. The proposed change was submitted to the NRC by

20

Letter RNP-RA/95-0214 on December 11, 1995, and was granted in Amendment

175. The amendment allows for the licensee one hour to meet the minimum

degree of redundancy. These LERs were closed.

III. Engineering

El

Conduct of Engineering

E1.1 Design Change Processes

a. Inspection Scope (37550)

The inspectors reviewed the licensee's procedures which control the

design change program to determine if the licensee was properly

controlling the design basis of the plant.

b. Observations and Findings

The inspectors reviewed the procedures listed below which control design

and design changes to determine if the procedure implement the

requirements of 10 CFR 50, Appendix B, Criterion III and 10 CFR 50.59.

The following procedures were reviewed:

.EGR-NGGC-001, Conduct of Engineering Operations, Rev. 1,

dated June 28, 1996

EGR-NGGC-003, Design Review Requirements, Rev. 0, dated June

3, 1996

EGR-NGGC-005, Engineering Service Requests, Rev. 2, dated

November 7, 1996, and,

EGR-NGGC-0304, Maintenance of Design Documents, Rev.0, dated

November 11, 1995.

The EGR-NGGC series of procedures were corporate level procedures

being issued to standardize engineering work activities at all

three CP&L nuclear plants. However, the inspectors noted that

when the new EGR-NGGC procedures were issued to improve design

control activities, previously issued procedures which they were

meant to replace were not deleted and/or canceled. For example,

EGR-NGGC-005 was issued to replace procedures PLP-064 and MOD-022.

The inspectors noted that PLP-064 and MOD-022 were still being

maintained current. Discussions with licensee engineers disclosed

that these procedures will be superseded and deleted from the

licensee's document control system in the near future. EGR-NGGC

005, Engineering Service Requests, streamlined the process for

performing engineering work.

The inspectors concluded that the new procedures adequately

addressed: design input, training, drawing changes, post-

21

modification testing, control of field changes, 10 CFR 50.59

safety evaluations, and ALARA reviews. However, review of EGR

NGGC-005 disclosed the following problem:

EGR-NGGC-005 defines

three types of engineering service requests (ESRs) which is the

process used for performing engineering work. These are design

change (DC), configuration change (CC), and engineering

disposition (ED) ESRs. Design change ESRs were defined as a

change which affects the design input of a system, structure, or

component (SSC), while a configuration change was a change to a

SSC which does not change the design inputs. Engineering

disposition ESR were used to supply information and did not

produce design output documents or change any SSC. ESRs

designated as design change ESRs require design verification to

meet the requirements of 10 CFR 50 Appendix B, Criterion III, ANSI

N45.2.11, and Regulatory Guide 1.64. ESRs designated as

configuration changes require an engineering review, instead of a

design verification. The engineering review, as defined.by CP&L

procedure EGR-NGGC-003 does not meet the in-depth review and

independent review requirements as defined by Appendix B,

Criterion III, ANSI N45.2.11, and Regulatory Guide 1.64. Pending

further review of the licensee's engineering review requirements,

this issue was identified as URI 50-261/96-14-01, Review

Licensee's Design Verification Requirements.

c. Conclusions

With the exception of the issue identified in URI 50-261/96-14-01, the

inspectors concluded that the licensee's design change control

procedures complied with the requirements of 10 CFR 50.59, and 10 CFR

50, Appendix B, Criterion III.

However, the inspectors noted that

duplicate procedures exist which could possibly result in confusion in

the future and could result in potential design errors. Further, a

process was in place that used an engineering review in lieu of a design

verification for plant changes designated as configuration changes only.

This practice does not appear to meet the requirements of 10 CFR

Appendix B and another regulatory guidance.

E1.2 Review of Design Changes and Modification Packages

a. Inspection Scope (37550)

The inspectors reviewed the design change and modification packages to:

(1)

determine the adequacy of the safety evaluation screening and the 10

CFR 50.59 safety evaluations; (2) verify that the modifications were

reviewed and approved in accordance with Technical Specifications and

administrative controls; (3) verify that applicable design bases were

included; (4) verify that Updated Final Safety Analysis Report

requirements were met;

(5) verify that both installation testing and

post modification testing requirements were specified so that adequate

testing would be accomplished.

22

b. Observations and Findings

The inspectors reviewed the following design change and modification

packages:

ESR-9500870:

PORV Block Valve Stem Replacement,

.ESR-9500782:

Resolve GIP Issues for RFO 17,

ESR-9600579:

MSIV Evaluation,

ESR-9600538:

ECCS Sump Screen -

Functional and Structural

Evaluation, and,

ESR-9600375:

Provide Input on EDG Fuel Oil Storage Tank

Level.

The inspectors found that the modification packages had been

reviewed and approved in accordance with the licensee's design

control procedures and that the format and content of the

modification packages was consistent with the design control

procedure. The quality of the modification packages was good.

c. Conclusions

In general, the modification packages were judged to be of good

quality and would not degrade plant performance, safety, or

reliability. The modification packages contained sufficient

specifications, drawings and procedures to be properly installed

and tested. The licensee's 10 CFR 50.59 evaluations were completed

in accordance with NRC requirements.

E2

Engineering Support of Facilities and Equipment

a. Inspection Scope (37550)

The inspectors performed a walkdown inspection of safety-related

structures and reviewed engineering involvement in maintaining

material condition of safety-related structures, systems, and

components.

b. Observations and Findings

The initial point of contact for maintenance personnel to obtain

engineering assistance is the RESS rapid response team. The

purpose of the rapid response team is to respond to emergent

issues, and to provide engineering assistance to plant personnel.

The rapid response team is involved directly in day-to-day

maintenance activities. The rapid response team has been recently

reorganized to include the predictive maintenance, preventative

maintenance, and thermal performance programs.

23

The inspectors, accompanied by a licensee engineer from the rapid

response team, walked down the auxiliary, control, containment,

and fuel handling buildings and examined plant material condition

and the condition of plant equipment. During the walkdown, the

inspectors noted that plant material condition was good to

excellent. There was no evidence of degraded operating equipment;

however, a few minor deficiencies were observed in containment

building. These included the presence of a rag, piece of duct

tape, pieces of string and other miscellaneous loose items in the

containment. Minor damage to the sheet metal waterproof barrier

covering the containment liner plate insulation was also noted.

The damage to the waterproof barrier included damaged/buckled

sheet metal panels and deteriorated caulking between numerous

sections of sheet metal and at the floor line. EBASCO

specification No. CPL-R2-M-18 and drawing G-190343 required the

liner insulation to be positively sealed against moisture. The

specification also required periodic monitoring of the presence of

moisture between the insulation and the liner plate. The purpose

of monitoring for moisture is to prevent corrosion of the liner

plate.

Discussions with licensee engineers disclosed that problems with

the sheet metal panels and containment liner corrosion were

documented in Engineering Evaluation EE-93-159 which was closed in

May, 1994. Some corrosion damage to the containment liner plate

was observed and evaluated. The inspectors reviewed the general

required actions list to close the engineering evaluation. These

included issuing of a work request (number WR 94-AHRZ1) which

required removal of additional panels for inspection of the liner

for potential corrosion during the next scheduled refueling outage

(refueling outage 16).

The inspectors reviewed the work request

and noted that it had been canceled (deleted) without the required

inspections being performed. Licensee engineers were unable to

provide any justification for not performing the liner

plate/insulation inspections. Paragraph 5.14.5.1 of CP&L

procedure MOD-001 Engineering Evaluation Rev. 1 requires the

engineering evaluation (EE) to be revised if the intent of the

required actions to close the EE are changed. Paragraph 5.9.2 of

CP&L procedure MMM-003 Maintenance Work Request requires the

reason for cancellation of a work request to be documented on the

work request. Failure to revise the engineering evaluation when

the intent of the required actions (perform additional inspections

of the containment vessel liner plate for corrosion damage) were

changed, and failure to document the reason for cancellation of

the work request was identified to the licensee as a violation of

10CFR50, Appendix B, Criterion V, failure to follow procedures.

This issue was identified as Violation 50-261/96-14-02, Failure to

Complete Corrective Actions to Resolve Containment Liner Corrosion

per Engineering Evaluation. The licensee initiated Condition

Report No. 96-03023 to followup on the condition of the liner

insulation and degraded panels.

24

c. Conclusions

A violation was identified regarding failure to follow procedure

in canceling corrective actions required by an engineering

evaluation. However, the inspectors concluded that licensee

engineers are actively involved in day-to-day support of plant

equipment. The material condition of the plant and equipment is

good to excellent.

E5

Training and Qualification of System Engineers

a. Inspection Scope (37550)

The inspectors reviewed the licensee's program for training and

qualification of plant (system) engineering personnel to assure

the quality of engineering training.

b. Observations and Findings

The inspectors reviewed the following procedures which specify the

requirements for training of engineering personnel:

Training Program Procedure TPP-213, Engineering Support

Personnel Training Program, Rev. 5, dated July 17, 1996

Technical Support Management Manual TMM-105, System Engineer

Certification Procedure, Rev. 2, dated April 20, 1996

These procedures establish the guidelines for training and

certification of personnel in the Robinson Engineering Support

Section (RESS).

Individual training schedules have been developed

for all RESS engineers which document required training, training

completed to date, and the scheduled completion dates for any

remaining training. The training includes initial orientation

training and position specific training for each engineer assigned

to RESS. After completion of their required training, the

engineers will receive certification as plant engineers. The

plant engineers will be responsible for both system design and

operation/maintenance. The inspectors reviewed the training

guides for individual engineers and noted that almost all

engineers are scheduled to be fully qualified as plant engineers

by June 1997.

c. Conclusions

The inspectors concluded that the licensee's program for training

and qualification of system engineers meets NRC requirements.

25

E7

Quality Assurance in Engineering Activities

E7.1 Special UFSAR Review

A recent discovery of a licensee operating their facility in a manner

contrary to the UFSAR description highlighted the need for a special

focused review that compares plant practices, procedures and/or

parameters to the UFSAR descriptions. While performing the inspection

discussed in this report, the inspectors reviewed selected portions of

the UFSAR that related to the areas inspected. The inspectors verified

that for the select portions of the UFSAR reviewed, the UFSAR wording

was consistent with the observed plant practices, procedures and/or

parameters.

E8

Miscellaneous Engineering Issues (37551 and 92903)

E8.1 (Closed) LER 50-261/94-18-01, -02, Technical Specification 3.0:

Containment Spray System: These LERs involved the licensee's entries

into TS 3.0 to sample the concentration of sodium hydroxide downstream

of the Containment Spray System (CSS) Spray Additive Tank (SAT)

discharge valves. The purpose of the sampling was to verify that sodium

hydroxide from the SAT was not leaking past the discharge valves. The

sample was obtained from a drain valve on the SAT eductor line after

aligning a 2-inch Refueling Water Storage Tank (RWST) line to the SAT

eductor piping. The licensee performed this sampling in conjunction

with the performance of CSS Inservice pump testing. In August 1994, the

licensee recognized that this sampling alignment resulted in the

potential inoperability of both trains of CSS since water from the

2-inch RWST line would be educted along with sodium hydroxide from the

SAT. This could result in reduced concentration of sodium hydroxide to

the suction of both CSS pumps should -a

CSS actuation signal occur.

Sodium hydroxide is used in the CSS to remove Iodine from the

containment atmosphere during design basis accidents. The licensee

determined that this sampling lineup potentially rendered the Iodine

removal function of the CSS inoperable, since the design concentration

of sodium hydroxide could not be assured to CSS pumps. As a result of

the potential inoperability of both trains of CSS, the licensee entered

the action requirement of TS 3.0 during the pump testing and sampling

evolutions until this issue could be resolved.

The licensee's corrective actions included performing an evaluation to

determine the effect of delaying the addition of sodium hydroxide to the

containment atmosphere on the control room operator 30-day thyroid dose

following an accident. The inspectors reviewed the results of this

evaluation which were documented in Calculation RNP-M/MECH-1592, Rev. 0.

General Design Criteria (GDC) 19 limits the 30-day thyroid dose to the

control room operators to 30 Rem. The results of the licensee's

calculation indicated that sodium hydroxide could be delayed by as much

as 6 minutes without exceeding the 30 Rem regulatory limit. However,

this delay would result in a slight increase from the previously

calculated control room operator dose of 27.3 Rem to 29.7 Rem. At the

end of the inspection period, the inspectors had not completed a

26

detailed review of the methodology used in the calculation to ensure

that it was acceptable. Pending completion of this review, this item

will be tracked as Part 1 of Unresolved Item (URI) 50-261/96-14-03:

Review Aspects of Containment Spray Additive Tank Eductor Line Sampling.

Using the results from the revised control room operator dose

calculation, the licensee determined that continued sampling using this

alignment could be performed without rendering the Iodine removal

function of the CSS inoperable as long as the SAT could be returned to

its normal alignment within 6 minutes. The licensee revised the CSS

pump test procedure, as well as other procedures where the sampling was

conducted, to add procedural controls for returning the SAT to its

normal alignment within 6 minutes of a CSS actuation signal.

The

inspectors reviewed Operations Surveillance Test (OST)-352, Containment

Spray Pump Test, Rev. 31, dated January 12, 1995, which incorporated

these changes. The inspectors determined that detailed guidance was

added to ensure that manual operator actions were completed to realign

the SAT to its normal lineup should a CSS actuation signal occur. The

inspectors verified that these actions were performed properly on

December 17, 1996, while witnessing the inservice testing of the "B"

CSS

pump.

Upon review of the 10CFR50.59 evaluation for OST-352, Rev. 31. the

inspectors questioned whether it was adequate. Specifically, the

inspectors questioned whether the change to the procedure constituted an

unreviewed safety question which would require NRC review and approval

prior to implementation. The inspector noted that this change might be

considered an unreviewed safety from several perspectives. First, based

on review of the UFSAR and TSs, the sampling evolution was not required

by. nor discussed in either of these licensing documents. Based on

this, the evolution might be considered a new "test" (i.e., leak check

of the SAT discharge isolation valves), which would make the change an

unreviewed safety question. Secondly, the licensee stated in their

evaluation that the change did not create the possibility of a

malfunction of equipment important to safety of a different type than

any evaluated previously in the Safety Analysis Report (SAR). The

inspectors.disagreed with this conclusion since failure of the operator

to close the manual RWST valve and failure of this manual valve to open

due to mechanical failure both introduce new failure modes which could

result in an increase in the probability of malfunction of the CSS

Iodine removal function. Thirdly, the licensee stated that the change

did not reduce the margin of safety as defined in the basis of the TSs

or increase the consequences of an accident evaluated previously in the

SAR. The inspectors disagreed with these conclusions since the

licensee's recalculation of control room operator dose showed that there

would be an increase from the current control room operator dose value

that was referenced in the SAR as a result of allowing a 6 minute delay

in sodium hydroxide to the containment atmosphere. At the end of the

report period, the inspectors were still discussing with the licensee

and NRR personnel specifics with regard to the adequacy of this

10CFR50.59 evaluation. The inspectors determined that further NRC

review of this issue was necessary, as such, this issue will be tracked

27

as Part 2 of URI 50-261/96-14-03: Review Aspects of Containment Spray

Additive Tank Eductor Line Sampling.

The inspectors discussed with engineering personnel the origin of the

SAT eductor line sampling evolution. The licensee initiated the

sampling evolutions in 1988 after it was identified that one of the SAT

discharge valves leaked by causing the contamination of sodium hydroxide

in the RWST and RCS. The licensee determined that continued sampling

was necessary to prevent recurrence of this incident. However, based on

inspector discussions with engineering personnel, they could not recall

any further incidents since 1988-89 where sample results had identified

similar leakage. This was attributed in part to repairs performed on

the SAT discharge valves which improved their leak tightness. The

inspectors questioned whether the licensee had evaluated other sampling

options or configurations and if it was still considered prudent to

perform this sampling evolution using such an undesirable configuration.

At the end of the report period, the inspectors were continuing

discussions with the licensee on the justification for continuing with

the present sampling configuration in lieu of other options which did

not challenge the operability of the CSS iodine removal function. This

will be tracked as Part 3 of URI 50-261/96-14-03: Review Aspects of

Containment Spray Additive Tank Eductor Line Sampling.

The LERs were closed based on tracking the issues identified from this

review via URI 50-261/96-14-03.

E8.2

(Closed) LER 50-261/95-02-00, Inadvertent Main Steam Isolation Valve

Closure During Plant Cooldown: On June 6, 1995, the unit was in Hot

Shutdown (231oF) and reactor coolant temperature decreasing to Cold

Shutdown (<2120F). A Main Steam Isolation signal was received which

caused an automatic closure of the Main Steam Isolation Valves (MSIVs),

which are Engineered Safety Features (ESFs). CR 95-01501 was initiated

to follow this item.

Investigation revealed that high steam flow bistables actuated with zero

steam flow indicated on the RTGB. The high steam flow signal was

created by a loss of water in the steam flow transmitter sensing line

which actuated the high steam flow bistables. An inspection of the

sensing line revealed that a portion of the line had been insulated

preventing radiant and convective heat loss. As a result, the water in

the sensing line flashed to steam as the operators decreased secondary

pressure to cool the plant.

The insulation was removed from the flow element ring headers of all

three steam generators to allow radiant and convective heat loss to

sustain condensation in the sensing lines during low steam line

temperature and pressure conditions. Labels were affixed to these lines

which specify that the lines should not be insulated. The licensee

revised General Procedure (GP)-007, Plant Cooldown From Hot Shutdown to

Cold Shutdown, in Revision 37 to preclude having the plant in the

condition-to receive these spurious actuations of the MSIVs.

28

The inspectors verified the placement of the signs on the sensing lines.

GP-007, Revision 37 was reviewed and the inspectors noted that Section

5.2.39 was changed to read reactor coolant temperature rather than steam

generator pressure and Section 5.2.39.8.d was added to close the MSIVs.

The inspectors reviewed GP-007, Revision 41 and verified that it

contains the same information. This item is closed.

E8.3

(Closed) LER 50-261/95-04-00, Reactor Trip Due To Main Steam Isolation

Valve Closure:

On June 30, 1995, a reactor trip occurred with the unit

operating at 100% power, as the result of an inadvertent closure of the

"B" Main Steam Isolation Valve (MSIV), MS-V1-3B. The closure of MS-V1

3B resulted in a Reactor Protection System (RPS) reactor trip signal

from Low-Low "B" Steam Generator Level.

The operators placed the unit

in Hot Shutdown in accordance with procedures. CR 95-01660 was

initiated to follow this event.

The followup investigation revealed that the MSIV closure was caused by

a loose fuse block fuse clip for the fuse that supplies control power to

the MSIVs actuator "open" air supply solenoid valve. A loss of power to

the solenoid valve occurred while an operator was reinstalling a fuse in

another circuit on the same fuse block. A second loose fuse clip was

identified during a panel walkdown.

The inspectors determined that on October 9, 1993, the licensee

experienced a short circuit between fuse clips which resulted in arcing

in a fuse block in the MSIV control cabinet. CR 93-00193 was initiated

to document the event. Corrective actions were to replace the fuse

blocks with a newer, more rigid design and review the event with the

operators. Engineering Service Request (ESR) 94-00543 was issued to

evaluate an improved design. Work Request (WR) 94-AHFQ1 was issued to

replace some of the older design fuse blocks. The work was scheduled

for Refueling Outage (RFO)-16 but subsequently deferred to RFO-17.

The licensee's corrective actions for the loose fuse clips included

replacing all the old design fuse blocks in accordance with the

resolution of ESR 94-00543 and reviewing the event with Operations and

Maintenance personnel.

WR 94-AHFQ1 was canceled and WRs 95-ALAJ1, 95

ALAK1, and 95-ALALl were issued to perform the work.

The inspectors reviewed CRs 93-00193 and 95-01660; training records;

ESR94-00543; and WRs 94-AHFQ1, 95-ALAJi, 95-ALAK, and 95-ALAL1. They

verified that the event had been reviewed with Operations and

Maintenance personnel. The review of the WRs which replaced the fuse

blocks indicated that the work had been completed between September 19

and 25, 1995. The licensee completed their corrective actions and this

item is closed.

29

IV. Plant Support

P2

Status of EP Facilities, Equipment, and Resources

P2.1 Facility Inspection

a. Inspection Scope (82701)

The inspectors toured the facilities to determine whether key facilities

and equipment were adequately equipped and maintained.

b. Observations and Findings

During the training drill on November 12, 1996, the inspectors toured

the Technical Support Center (TSC), Operational Support Center (OSC),

and Emergency Operations Facility (EOF) and observed the licensee's

facilities and equipment being utilize during the drill.

The

Telephones, fax machines, Safety Parameter Display System (SPDS),

Emergency Response Facility Information System (ERFIS), Dose Assessment

Computer, and the Emergency Notification Network (ENN) phone system

operated properly.

The inspectors reviewed surveillance records of emergency supplies and

equipment required in EPPRO-02, Maintenance and Testing. All

surveillances were performed at the required frequencies. The

documentation of the surveillances indicated that the licensee

maintained good control of their emergency supplies and that the

emergency equipment was reliable. No discrepancies were noted by the

inspectors. No significant changes had been made to the facilities.

c. Conclusion

The inspectors concluded that the facilities were well equipped and the

licensee maintained the facilities and equipment in a good level of

operational readiness.

P2.2 Emergency Response Dose Assessment Capabilities

a. Inspection Scope (82701)

Dose Assessment Capabilities were inspected to verify that the licensee

maintained continuous dose assessment capabilities which used real time

meteorological and radiological data.

b. Observations and Findings

The licensee's dose assessment program was on the Emergency Response

Facility Information System (ERFIS) computer. The inspector observed

the licensee's dose assessment program in operation during the training

drill.

The program was a straight line gaussian calculation which used

30

real time radiological and meteorological data which was automatically

updated and input into the program.

The licensee maintained Emergency Plan Implementing Procedure, EPRAD-03,

Dose Projection, for performing manual dose calculations. All licensed

operators were trained in both the computer and EPRAD-03 to perform

on-shift dose assessment.

c. Conclusion

The inspectors concluded that the licensees's dose assessment

capabilities were satisfactory and that sufficient personnel were

trained to perform onshift dose assessment using real time

meteorological and radiological data.

P2.3 Public Alert And Notification Capabilities

a. Inspection Scope (82701)

This area was inspected to review the licensee's method of notifying the

public in the event of an emergency, the notification test frequency,

and notification test data.

b. Observations and Findings

The licensee maintained 45 sirens within the Emergency Preparedness Zone

(EPZ) for their public alert and notification system. The licensee

performed a bi-weekly silent test, quarterly growl test, and an annual

sounding of the sirens. The 1995 Robinson Nuclear Plant siren

availability report summary indicated a siren availability of 98.5

percent.

The inspectors reviewed documentation of Robinson's siren testing from

October 1995, through October 1996 and determined that the sirens had

been tested at the required frequencies.

c. Conclusion

The inspectors concluded that the operational status and maintenance of

the siren system was good.

P3

EP Procedures and Documentation

P3.1 Maintenance of the Emergency Plan and Procedures

a. Inspection Scope (82701)

The inspectors reviewed the licensee's process for making changes to the

Emergency Plan and Plan Emergency Procedures (PEPs). The inspectors

reviewed changes to the PEPs to verify that the changes were in

agreement with and.implemented the Emergency Plan.

31

b. Observations and Findings

The inspectors compared the instrumentation ranges and nomenclature

identified in the Emergency Action Levels (EALs) to the installed

instrumentation in the Control Room. In the comparison, no

inconsistencies in nomenclature or in the use of terms were identified

by the inspectors. The inspectors verified that the EALs were reviewed

and agreed upon by the State.

The licensee had performed a detailed "word by word" annual review of

their Emergency Plan in Revision 34. Concurrently with Revision 34, the

licensee completely reviewed and re-organized their PEP's. In the

procedure reorganization, procedure identifiers were changed from PEP to

EP plus the facility or function identifier.

The inspectors reviewed Administrative Procedure AP-22, "Document Change

Procedures," the licensee's process for making changes to their Plan and

Plan Emergency Procedures (PEP), Plant Licensing Procedure PLP-032,

10 CFR 50.59 Reviews of Changes, Tests And Experiments, and the

licensee's re-organized emergency procedures. The inspector determined

that the re-organized procedures were in agreement with the plan, and

the licensee had followed AP-22 and PLP-32 in making the plan and

procedure changes.

The inspectors viewed the emergency procedure changes as a excellent

organizational and ergonomic improvement of the EPs.

The inspectors reviewed the change matrix associated with the EP's

re-organization and the change packages associated with the individual

EP changes and determined that they were satisfactory and followed AP-22

and PLP-032.

The process for making changes to the PEPs and the Emergency Plan met

the intent of 10 CFR 50.54(q).

All of the changes reviewed were approved and distributed in accordance

with the licensee's procedures. The NRC was notified within 30 days of

all changes as required in 10 CFR 50 Appendix E.

Controlled volumes of the EPs in the Technical Support Center (TSC),

Emergency Operations Facility, and Operational Support Center (OSC) were

reviewed and determine to be maintained up to date.

The inspectors reviewed the letters of agreement identified in

Appendix 6.2, "Agreement Letters", of the Emergency Plan and verified

that they were up-to-date.

c. Conclusion

The inspectors concluded that the licensee's Plan and procedure change

review process was thorough and met the requirements of 10 CFR 50.54(q).

The inspectors viewed the new designation and reorganization of the

32

emergency procedures as a excellent organizational and ergonomic

improvement.

P3.2 Use Of The Emergency Implementing Procedures

a. Inspection Scope (82701)

The inspectors reviewed the licensee's event declarations to verify that

each event was properly classified and the Emergency Implementing

Procedures were properly implemented.

b. Observations and Findings

Review of the licensee's 10 CFR 50.72 reports since September 1995,

revealed that the licensee had made one event declaration:

May 13, 1996, a Unusual event was declared due to a fire in the

mechanical equipment room of the chemistry building lasting

greater than ten minutes.

c. Conclusion

The inspectors review concluded that the licensee properly classified

the event.

P5

Staff Training and Qualification in EP

P5.1 Drill Observation

a. Inspection Scope (82701)

Observe a licensee training drill, their preparation, degree of play,

and critique.

b. Observations and Findings

Records reviewed showed that each of the five shift operating crews

drilled with one of the emergency response team in each of the three

cycles of their annual retraining. As a result of the licensee

combining licensed operator requalification training and emergency

preparedness training, the licensee plans to perform fifteen emergency

response drills this year.

The inspectors observed an Emergency Preparedness drill on November 19,

1996. The drill was observed as a training evolution rather than being

evaluated. The licensee had committed almost as much work in the

drill's planning and details as licensee's normally do for an evaluated

exercise. Scenario booklets were developed, pre-drill evaluator briefs

and post drill critiques were held. All of the facilities were

activated and functioned properly. As part of the scenario, the OSC was

relocated when the facilities habitability was challenged. The

licensee's critique following the scenario was objective. Issue's

33

identified during the critique were documented by the licensee as

improvement items or corrective actions, particularly in the Joint

Information Center.

c. Conclusion

The inspector concluded the licensee's combining of licensed operator

requalification training and emergency preparedness training was a

strength for the emergency preparedness program.

P5.2 Training of Emergency Response Personnel

a. Inspection Scope (82701)

The inspectors reviewed the Emergency Response Training Program and the

verified that emergency response personnel were initially trained and

retrained annually to maintain their training current.

b. Observations and Findings

The licensee's Emergency Preparedness training program EPPRO-03,

Training and Qualification was rewritten in October 1996. The inspector

interviewed staff personnel responsible for rewriting the program and

reviewed the changes between the old and new program. The new program

consolidated or reorganize lesson plans and course requirements for the

different positions. In the.two programs the same level of specific

information was being taught to the member, but the scope of information

presented had been expanded. The inspectors concluded that the new

program provided more flexibility to the licensee in cross training

Emergency Response Organization personnel and provided-broader training

for an individual ERO member. The inspector viewed the new program as a

program improvement.

Emergency Preparedness training consisted of initial training, annual

retraining, and continuing training. Initial training consisted of

respirator qualification if required, classroom instruction and testing,

reading the required procedures, job list, and observation or evaluation

of performance in drill or exercise. Annual retaining consisted of

reading the required procedures, job list and observation or evaluation

of performance in drill or exercise. Continuing training consisted of

classroom discussion prior to drills base upon training needs identified

during drills/exercise critiques, student feedback, and/or related

current industry events.

The inspectors reviewed the lesson plans and exams for the Overview,

TSC, and OSC. The inspectors noted from the review that the lesson

plans were organized and contained the appropriate depth of material.

The exams could be improved upon. The exams were multiple choice and

contained negative learning questions (were the student is asked to

chose the wrong answer), poor distractor (obvious wrong answers), and

instances in which the question asked was the answer to the preceding

question. The inspectors discussed the exams with the licensee. The

34

licensee stated that they intended to re-write the exams as part to the

program upgrade.

The status of ERO training was reviewed by randomly selecting ten

individuals from the ERO and reviewing their training records. The

training for all of the individuals reviewed by the inspectors was

up-to-date. The licensee continued to maintain ERO training in

accordance with their Emergency Plan and EPPRO-03.

c. Conclusion

The inspectors concluded that the licensee was effectively implementing

the ERO training program.

P5.3 Emergency Planning Drills

a. Inspection Scope (82701)

The inspectors compared the licensee's drill commitments to the actual

drills performed, and evaluated the quality of those drills.

b. Observations and Findings

Three scenarios were used in fifteen drills during the year. One

scenarios was used for each of the three cycles of licensed operator

training.

The inspectors reviewed the documentation from six of the licensee's

drills. The scenarios were challenging, and the licensee's evaluation or

critiques of the drills were objective. The drill comments were well

documented, tracked, and resolved.

The inspectors reviewed the licensee's matrix of their exercise

elements. The matrix identified required exercise elements and the last

time the element was exercised. The matrix corresponded to the elements

identified in the guidance of NUREG-0654, "Criteria for Preparation and

Evaluation of Radiological Emergency Response Plans and Nuclear Power

Plants" and NUREG-0737, "Clarification of TMI Action Plan Requirements."

As a minimum, each element was to be exercised once every six years.

All exercise element requirements were currently satisfied.

c. Conclusion

The license's conduct of drills exceeded their commitment in their

Emergency Plan. The combining of licensed operator retraining with

emergency preparedness drills, the number of drills performed during the

year, the level of participation, and the feedback provided to the

players was a strength.

35

P6

EP Organization and Administration

a. Inspection Scope (82701)

The inspectors reviewed this area to determine if any changes in

management or personnel had occurred which would effect the efficiency

or performance of the Emergency Response Organization.

b. Observations and Findings

The manager responsible for the emergency preparedness programs

direction and support recently changed. No significant changes had

occurred which negatively affected the performance or maintenance of the

Emergency Preparedness Program as a result of that change. During the

inspection, the inspectors observed several areas that indicate that

emergency preparedness was receiving strong management support.

Examples were:

Upgrading of the siren system,

Personnel and time committed to drills and training,

Rewriting or reorganizing of the emergency procedures, and

Rewriting or reorganizing of the training program.

c. Conclusion

No changes occurred had which affected the performance of maintenance of

the Emergency Preparedness Program. Emergency Preparedness was

receiving strong management support.

P7

Quality Assurance of EP Activities

P7.1 Required 10 CFR 50.54(t) Audit Of Emergency Preparedness Program

a. Inspection Scope (82701)

The inspectors reviewed this area to assess the quality of the required

audit, the qualification of the auditors, and verify that the audit met

the requirements of 10 CFR 50.54(t).

b. Observations and Findings

The inspector reviewed Audit Report R-EP-95-02 and draft Audit Report

R-EP-96-01. Audit Report R-EP-95-02 was a six person team audit

conducted in November 1995 and identified one strength, one issue, and

three weaknesses. Audit Report R-EP-96-01 was a six person team audit

conducted in October 1996 and identified one potential issue, and one

potential weakness.

36

After reviewing audit report R-EP-95-02 and draft audit report

R-EP-96-01, the inspector reviewed the assessment outlines that had been

developed prior to each of the audits. The inspector noted that the

outlines were detailed and well organized. Audit areas were clearly

defined and the elements used to audit the different areas were detailed

and of sufficient scope to perform a thorough audit of the area.

After reviewing the audit summaries and assessment outlines, the

inspectors interviewed the Lead Auditor and reviewed the auditor's

elements and notes. The inspectors concluded from the interview and

review of the auditor's notes that the scope and depth of the audit

satisfactorily covered the elements required by 10 CFR 50.54(t) for an

annual independent audit of the Emergency Preparedness program.

The inspectors reviewed the qualification and training, of the auditors

and lead auditor. The auditor's qualifications met the licensee's

Quality Audit program requirements.

c. Conclusion

The inspectors concluded that the auditors' qualifications were good,

and the scope of the audit was good. The audit satisfied the 10 CFR

50.54(t) requirement for an annual independent audit of the EP program.

P7.2 Licensee's Corrective Action Program For Drill Comments and Issues

a. Inspection Scope (82701)

The area was inspected to evaluate the licensee's corrective action to

comments and issues identified in their drills.

b. Observations and Findings

The inspectors reviewed findings from audits, inspection reports,

and exercise and drill critiques. These findings were compared to

the issues identified in the licensee's CAP.

The inspectors selected eight completed packages from the emergency

preparedness CAP list for a more detailed review. The packages were

reviewed to evaluate the licensee's responsiveness to resolving issues

and the adequacy of their closure. From the packages reviewed, the

inspectors determined that the licensee was responsive in addressing

emergency preparedness issues and that the closure resolutions were

adequate.

The licensee stated that they maintained a separate emergency

preparedness tracking list for emergency preparedness issues (drill

critiques) which do not rise to the level of the CAP program. The

licensee stated that they were transferring the list from a "hard copy"

to a computer based list, and that while upgrading the site's computer

systems, the program was lost. The licensee was in the process of

restoring their lower level tracking system. The inspectors selected

37

several issues that had been identified in drill critiques and were not

in the CAP program, and verified they had been corrected.

Documentation had been identified as concerns in a previous NRC

inspection and in Audit Report R-EP-95-02. Other examples of missing

documentation note by the inspector during this inspection were:

First semi-annual PASS drill,

Two letters of agreement, and

Corrected pages in procedure change form documentation.

c. Conclusions

The emergency preparedness organization was adequately tracking and

resolving upper tiered issues through the CAP program. The licensee's

loss of their lower level tracking system contributed to continuing

problems with documentation. Control of documentation continues to be a

concern.

V. Management Meetings

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee

management at the conclusion of the inspection on January 6, 1997.

Interim exits were conducted on November 22 and 27, and December 6,

1996. The licensee acknowledged the findings presented.

The inspectors asked the licensee whether any materials examined during

the inspection should be considered proprietary. No proprietary

information was identified.

38

PARTIAL LIST OF PERSONS CONTACTED

Licensee

H. Chernoff, Supervisor, Licensing/Regulatory Programs

J. Clements, Manager, Site Support Services

D. Crook, Senior Specialist, Licensing/Regulatory Compliance

C. Hinnant, Vice President, Robinson Nuclear Plant

J. Keenan, Director, Site Operations

B. Meyer, Manager, Operations

G. Miller, Manager, Robinson Engineering Support Services

R. Moore, Manager, Outages/Scheduling

J. Moyer, Manager, Maintenance

D. Stoddard, Supervisor, Operating Experience Assessment

R. Warden, Manager, Nuclear Assessment Section

T. Wilkerson, Manager, Environmental Control

D. Young, General Manager, Robinson Plant

NRC

B. Desai, Senior Resident Inspector

J. Zeiler, Acting Senior Resident Inspector

P. Byron, Resident Inspector, Surry

39

INSPECTION PROCEDURES USED

IP 37550:

Engineering

IP 37551:

Onsite Engineering

IP 40500:

Evaluation of Licensee Self-Assessment Capability

IP 61726:

Surveillance Observations

IP 62707:

Maintenance Observation

IP 71707:

Plant Operations

IP 82701:

Operational Status Of The Emergency Preparedness Program

IP 92901:

Followup - Operations

IP 92902:

Followup - Maintenance

IP 92903:

Followup - Engineering

ITEMS OPENED, CLOSED, AND DISCUSSED

Opene

Typ

Item Number

Status

Description and Reference

URI

50-261/96-14-01

Open

Review Licensee's Design Verification

Requirements (Section E1.1)

VIO

50-261/96-14-02

Open

Failure to Complete Corrective Actions to

Resolve Containment Liner Corrosion per

Engineering Evaluation (Section E2)

URI

50-261/96-14-03

Open

Review Aspects of Containment Spray

Additive Tank Eductor Line Sampling

(Section E8.1)

Closed

jp Item Number

Status

Description and Reference

VIO

50-261/95-21-01

Closed

Operator Failure To Monitor Plant Status

(Section 08.1)

VIO

50-261/95-27-01

Closed

Inadequate Clearance Results In Unexpected

Emergency Diesel Start (Section 08.2)

VIO

50-261/96-01-01

Closed

Auxiliary Feedwater System Valve

Misalignment (Section 08.3)

VIO

50-261/95-19-05

Closed

RHR Pump Start Due to Troubleshooting

(Section M8.1)

LER

50-261/95-06-00

Closed

Technical Specifications Violation Due To

Failure To Meet Minimum Degree Of

Redundancy (Section M8.2)

40

LER

50-261/95-07-00

Closed

Condition Prohibited By Technical

Specifications Due To Failure To Meet

Minimum Degree Of Redundancy (Section

M8.2)

LER

50-261/95-07-01

Closed

Condition Prohibited By Technical

Specifications Due To Failure To Meet

Minimum Degree Of Redundancy (Section

M8.2)

LER

50-261/95-08-00

Closed

Condition Prohibited By Technical

Specifications Due To Failure To Meet

Minimum Degree Of Redundancy (Section

M8.2)

LER

50-261/94-18-01

Closed

Technical Specification 3.0: Containment

Spray System (Section E8.1)

LER

50-261/94-18-02

Closed

Technical Specification 3.0: Containment

Spray System (Section E8.1)

LER

50-261/95-02-00

Closed

Inadvertent Main Steam Isolation Valve

Closure During Plant Cooldown (Section

E8.2)

LER

50-261/95-04-00

Closed

Reactor Trip Due To Main Steam Isolation

Valve Closure (Section E8.3)