ML14181A847

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Insp Rept 50-261/96-11 on 960818-0928.Violations Noted:Major Areas Inspected:Licensee Operations,Maint,Engineering & Plant Support
ML14181A847
Person / Time
Site: Robinson 
Issue date: 10/25/1996
From:
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14181A845 List:
References
50-261-96-11, NUDOCS 9611040306
Download: ML14181A847 (38)


See also: IR 05000261/1996011

Text

U.S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket No:

50-261

License No:

DPR-23

Report No:

50-261/96-11

Licensee:

Carolina Power & Light (CP&L)

Facility:

H. B. Robinson Unit 2

Location:

2112 Old Camden Rd.

Hartsville, SC 29550

Dates:

August 18 - September 28. 1996

Inspectors:

J. Zeiler, Acting Senior Resident Inspector

P. Byron, Resident Inspector

B. Desai, Senior Resident Inspector

G. Kuzo, Region II Inspector (R1.2, R1.3, R2,

R5, and R7)

M. Miller, Region II Inspector (M1.2)

C. Rapp, Region II Inspector (E8.1 and E8.2)

Approved by:

M. Shymlock. Chief. Projects Branch 4

Division of Reactor Projects

Enclosure 2

9611040306 961025

PDR ADOCK 05000261

a

PDR

EXECUTIVE SUMMARY

H. B. Robinson Power Plant, Unit 2

NRC Inspection Report No. 50-261/96-11

This integrated inspection included aspects of licensee operations,

maintenance, engineering, and plant support. The report covers a six-week

period of inspection; in addition, it includes the results of a maintenance,

service water followup, and effluents and radiological transportation

inspections by three Region II inspectors.

Operations

The licensee's preparations for Hurricane Fran were thorough. Although

activities were complicated by the considerable amount of equipment and

material which had been pre-staged onsite for the start of an upcoming

refueling outage. licensee management demonstrated conservative decision

making in removing and/or securing this material (Section 01.2).

The plant shutdown to begin Refueling Outage 17 was controlled and

conducted in a safety conscious manner. The operators followed the

applicable procedures and appropriately responded to plant problems

encountered (Section 01.3).

The decision to manually trip the reactor after encountering a turbine

Electro-Hydraulic Control System malfunction during unit shutdown was

justified.

Operator response to the trip was good and unit

stabilization was accomplished in a controlled manner. The root cause

of the trip was adequately identified and corrected. Adequate

resolution was performed or was planned prior to restart for other

unexpected plant equipment operation during or following the trip

(Section 01.4).

Reactor coolant system drain down activities were conducted in a

deliberate and controlled manner. A thorough pre-job briefing was

performed prior to the evolution. Important plant indications were

closely monitored by the operators (Section 01.5).

Fuel off-load activities were performed in a controlled manner. Good

communications were maintained between the Control Room and fuel

building operators (Section 01.6).

The first example of a violation of Technical Specification (TS)

6.5.1.1.1 was identified for failure to follow foreign material

exclusion area (FMEA) procedural requirements resulting in a loss of

control of foreign material exclusion inside the Spent Fuel Pool

Building during fuel off-load activities.

Ineffective supervisory

overview contributed to this problem. These deficiencies were similar

to previous problems indicating a continuing trend of ineffective FMEA

implementation requirements (Section 01.7).

An Auxiliary Operator was assigned five shifts as a Fire Brigade member

with an expired medical examinahion. Previous corrective actions to

ensure that operator medical qualifications were current prior to

2

individuals standing Fire Brigade and Control Room Shift Supervisor

watch duties were inadequate. This issue was identified as a Violation

of 10 CFR 50. Appendix B, Criterion XVI. for inadequate corrective

actions (Section 01.8).

Maintenance

The second example of a violation of TS 6.5.1.1.1 was identified when a

contractor electrical technician failed to follow modification procedure

requirements for obtaining operations permission and tagout clearances

prior to cutting power cables to valve SI-866A. This resulted in the

cable being cut while still energized. The licensee's stand down to

reemphasize work control expectations and requirements following this

and one other significant outage related work control error was

effective in preventing further serious problems (Section M1.1).

The maintenance and engineering departments were in the process of

implementing a thorough program to identify and correct repetitive

equipment failures (Section M1.2).

Engineering

Investigations of the A Main Steam Isolation Valve failure to close

during shutdown were thorough. The root cause was adequately addressed

and corrective actions planned were determined to be acceptable (Section

E1.1).

Plant Support

Radiological controls associated with low-level radioactive solid waste

stored temporarily on site met 10 CFR Part 20 requirements. Posting.

labeling, and physical controls for locked high radiation and very high

radiation area doors met regulatory requirements. Occupational

radiation exposure controls and evaluations for "hot particles" and for

potential internal exposure were adequate (Section R1.1).

One Non-Cited Violation of TS 6.11 for failure to follow radiation

protection procedures was identified. A breakdown in communication

among Health Physics technician staff contributed to contamination being

released offsite (Section R1.2).

Transportation and packaging activities for radioactive waste or

material shipments met 10 CFR 71.5 and 49 CFR requirements. Revised

Department of Transportation (DOT) guidance was properly implemented.

Training of personnel on the revised guidance was adequately performed

(Sections R1.3 and R5.1).

Audits of radioactive waste, effluent and transportation program

activities were thorough and met TS, 10 CFR Parts 20 and 71

requirements. Quality control activities associated with effluent

measurements were technically adequate (Sections R2.2. R7.1 and R7.2).

3

Actions to resolve a signal transmission problem with the public warning

system sirens following passage of Hurricane Fran were adequate (Section

P2.1).

The third example of a violation of TS 6.5.1.1.1 was identified

involving a discrepancy in the emergency procedure for performing off

site dose projections from the Control Room during accident conditions

involving releases of radioactive material (Section P3.1).

2

against high winds, stringing of hand lines for pre-established routes

to be used during the hurricane. verifying the operability of plant

equipment and components, and testing certain plant equipment such as

the emergency and dedicated shutdown diesel generators to ensure their

availability in the event offsite power were lost.

The inspectors reviewed the completed procedure attachment and conducted

an independent walkdown of the site to verify that preparations were

adequately implemented. The inspectors noted that licensee actions to

remove or secure items were aggressively pursued. All hurricane

preparations were completed on September 5. at 2:45 p.m. These

activities were well coordinated and thorough. even though they were

complicated by the large amount of material and equipment that had

recently been pre-staged for the upcoming refueling outage. Management

demonstrated conservative decision making in determining what pre-staged

material was removed and/or secured.

Based on weather projections that hurricane force winds would not be

expected near the site, management decided that a plant shutdown was not

necessary. On September 5, at approximately 8:00 p.m., the hurricane

made landfall several hundred miles to the north of the site, traveling

north-northwest. Maximum sustained winds of approximately 30-40 mph

were observed at the site, however, no significant damage occurred

onsite. Offsite power and communications were maintained throughout the

storm.

c. Conclusions

The inspectors concluded that the licensee's readiness for the

Hurricane's arrival was well coordinated and thorough. Management

demonstrated conservative decision making in determining what outage

pre-staged material was removed and/or secured onsite.

01.3 Shutdown for Refueling Outage Activities

a. Inspections Scope (71707)

The inspectors monitored shutdown activities that were conducted

September 7 to begin RFO-17. The shutdown was performed in accordance

with General Procedure GP-006. Normal Plant Shutdown from Power

Operation to Hot Shutdown. rev. 27.

Report Details

Summary of Plant Status

Unit 2 remained at essentially full power until August 27, when a coastdown

was initiated in preparation for starting Refueling Outage 17 (RFO-17). On

September 7. the unit commenced the outage shutdown from 89 percent power.

During the shutdown, a manual reactor trip was initiated from 28 percent power

after a turbine control system malfunction. Following the reactor trip, the

unit was placed in cold shutdown for refueling. On September 17. fuel off

load was completed and fuel remained removed from the core for the remainder

of the report period.

I. Operations

01

Conduct of Operations

01.1 General Comments (71707)

The inspectors conducted frequent control room tours to verify proper

staffing, operator attentiveness and communications, and adherence to

approved procedures. The inspectors attended daily operations turnover,

management review, and plan-of-the-day meetings to maintain awareness of

overall plant operations. Operator logs were reviewed to verify

operational safety and compliance with Technical Specifications (TSs).

Instrumentation, computer indications, and safety system lineups were

periodically reviewed from the Control Room to assess operability.

Frequent plant tours were conducted to observe equipment status and

housekeeping. Condition Reports (CRs) were routinely reviewed to assure

that potential safety concerns and equipment problems were reported and

resolved.

In general, the conduct of operations was professional and safety

conscious. Good plant equipment material conditions and housekeeping

was noted throughout the report period. Specific events and noteworthy

observations are detailed in the sections below.

01.2 Preparations for Hurricane Fran

a. Inspection Scope (71707, 71750)

Between September 4-6, the inspectors reviewed licensee preparations in

response for Hurricane Fran. This included a review of Operations

Management Manual (0MM) procedure OMM-021. Operation During Adverse

Weather Conditions, Rev. 15, and verification that the actions

prescribed by the procedure were properly implemented.

b. Observations and Findings

On September 4, at 7:15 a.m., the licensee began preparing for the

possible impact from Hurricane Fran. Preparations included completing

the actions for a hurricane warning in accordance with OMM-021,

Attachment 6.1. Hurricane Warning Check-off Sheet. Major activities

performed included: removal or securing loose material around the site

3

b. Observations and Findings

On September 7, at 8:30 p.m., the licensee commenced the shutdown in

accordance with GP-006. The inspectors monitored portions of the

shutdown from the Control Room. The inspectors verified that the proper

revision of the procedure was being used and that a pre-job brief was

performed prior to commencing activities. The inspectors noted.that

preparations were thorough and that activities were performed in a

controlled and deliberate manner. Both the Plant Manager and operations

management personnel were present in the Control Room and provided good

overview of the activities.

During the shutdown, steam flashing occurred while isolating the four

Moisture Separator Reheaters (MSRs). When the first shutoff valve (to

the 1A MSR) was closed, all four of the MSR Timer Valves automatically

reopened and admitted steam to the MSRs. As result of the sudden

increase in MSR pressure due to the introduction of steam, condensate

was suddenly introduced to the high pressure feedwater (HPFW) heaters

via the high level drain lines which were still open at the time.

During this pressure transient, one of the snubber supports on the high

level drain line from the lB MSR to the 6B HPFW Heater was damaged.

This pressure transient appeared to be a recurring incident in that GP

006 contained warnings that potential pressure spikes could occur when

the MSR shutoff valves were closed. A CR was initiated by the licensee

to address this apparent valve coordination problem and a work request

was initiated to repair the damaged snubber.

At approximately 30 percent power, the operators received a control room

alarm indicating that vibration of the No. 1 turbine-generator bearing

had increased to 6 mils.

The operators properly referred to the alarm

response procedures and followed the appropriate actions. The

procedures required that the turbine be tripped if vibration increased

to greater than 14 mils. Although vibration remained at 6 mils, the

operators remained diligent in monitoring for any subsequent vibration

increase.

At approximately 28 percent power, the operators encountered a problem

with the Turbine Electro-Hydraulic Control (EHC) System which prevented

the turbine from unloading properly. As a result of this problem, the

reactor was manually tripped. Following the trip, the operators

successfully stabilized the unit and continued the plant cooldown in

accordance with GP-007, Plant Cooldown from Hot Shutdown to Cold

Shutdown, rev. 41.

Further details of the EHC problem and operator

response to the trip is discussed in Section 01.4.

c. Conclusions

The inspectors concluded that the shutdown was controlled and conducted

in a safety conscious manner. The operators followed the applicable

procedures and appropriately responded to plant problems encountered.

4

01.4 Manual Reactor Trio due to Turbine Governor Valve Failure

a. Inspection Scope (71707, 93702 and 40500)

On September 7, while the plant was being shutdown to start RFO-17, the

Turbine EHC System failed to respond in either automatic or manual

control modes. As a result of this malfunction, a decision was made to

manually trip the reactor. The inspectors monitored the licensee's

response to the EHC System problem and discussed the problem and

decision to trip the reactor with the operators and plant management

personnel. The inspectors observed operator activities associated with

the manual trip and unit stabilization. In addition, the inspectors

reviewed post-trip plant data and attended the post trip assessment

conducted by the Plant Safety Review Committee (PNSC).

b. Observations and Findings

On September 7, the operators were conducting a scheduled shutdown to

begin RFO-17. At 10:41 p.m., with the unit operating at 28 percent

power, the EHC Turbine Control System malfunctioned in automatic mode,

preventing the complete closure of the remaining turbine governor valve

  1. 1 (GV-1). After placing turbine control in manual mode, the operators

were still unable to close GV-1. Following discussions between the

operators and operations management personnel who were present in the

control room to monitor the shutdown, a decision was made to manually

trip the reactor. This decision was based on xenon buildup in the core

and the risk of tripping the turbine if EHC system troubleshooting was

attempted.

At 11:13 p.m., the reactor was manually tripped from 28 percent power.

The reactor trip caused a turbine trip resulting in the closure of GV-1.

Following the trip, the unit was stabilized at no-load temperature and

pressure. Operator response to the trip was good: actions to stabilize

the unit were performed in accordance with the applicable emergency

procedures. The inspectors monitored plant parameters and equipment

operation to verify that safety systems responded as expected to the

trip. Two minor equipment problems were noted. Immediately following

the trip, the A Main Feedwater Pump tripped on low feedwater flow

resulting in the start of the motor driven Auxiliary Feedwater Pumps.

This was thought to have been caused by the slow opening of the A Main

Feedwater Pump recirculation valve to the condenser. In addition, the

control rod bottom indication lights associated with rods B-10 and H-8

did not initially illuminate. All control rods were confirmed to be

fully inserted, therefore, this was an indication problem only. The

inspectors reviewed the licensee's post trip review report completed

following the trip and verified that these items were captured and would

be resolved prior to unit restart. Following unit stabilization, plant

cooldown to cold shutdown was continued. At 11:54 p.m., the licensee

notified the NRC of the event. This iotification met the 4-hour

reporting requirement of 10 CFR 50.72 b)(2)(ii).

5

The licensee's investigation determined that the cause of the turbine

control malfunction was a broken wire in the EHC controls to GV-1. The

broken wire interrupted the electrical signal from the EHC System to the

valve controller for GV-1. The cause of the broken wire was determined

to be from fatigue as a result of repeated termination and de

termination of the wire from its housing terminal block during previous

maintenance activities. The broken wire was repaired and the controller

housings for all governor valves were inspected to ensure that no other

similar wire degradations existed. The inspectors determined that the

licensee had adequately addressed the root cause and corrective actions

of the EHC control problem.

On September 25. the inspectors attended the PNSC meeting during which

the root cause of the EHC control problem was discussed. The system

engineer responsible for the EHC system thoroughly discussed the problem

with the broken wire in the EHC controller housing, corrective actions

to repair the wire and inspections performed on the other valve control

housings. The inspectors noted that limited discussions were conducted

on details of the post trip review report or other equipment problems

identified following the trip. However, a PNSC action item was

identified requiring a more thorough review of these items prior to

plant startup.

c. Conclusions

The inspectors determined that the decision to trip the unit was

justified based on the risk with troubleshooting the EHC malfunction.

Operator response to the trip was good and unit stabilization was

accomplished in a controlled manner. The licensee adequately determined

the root cause of the trip and corrected the equipment related failure.

Adequate resolution was performed or was planned prior to restart for

other unexpected plant equipment operation following the trip.

01.5 Drain Down of the Reactor Coolant System

a. Inspection Scope (71707)

The inspectors verified readiness and observed Control Room activities

associated with the drain down of the reactor coolant system (RCS) to -7

inches (i.e.. 7 inches below the reactor vessel flange) in accordance

with GP-008, Draining the Reactor Coolant System. rev. 43.

b. Observations and Findings

Prior to the drain down, the inspectors verified the adequacy and use of

procedures and controls for the following: risk outage management. RCS

temperature and level instrumentation availability, containment closure

capability. RCS inventory addition capability, and emergency power

availability and protection. Specific details of this review are as

follows:

6

Shutdown Risk Management Controls:

The inspectors reviewed PLP-055, Outage Risk Management, rev. 13.

This procedure provided administrative controls and personnel

responsibilities for ensuring that actions governing safe plant

operation during RCS drain down and reduced inventory conditions

were conducted. The procedure provided safety system equipment

availability requirements for all shutdown conditions. Shutdown

safety equipment requirements were summarized on a one page matrix

that was updated and distributed twice a day to ensure that

personnel were cognizant of current shutdown conditions and

equipment requirements. In addition, signs were placed on safety

equipment required for current plant conditions warning personnel

that the equipment was being "protected." The inspectors

performed walkdowns of selected safety equipment to verify proper

material conditions and that the warning signs were installed in

accordance with PLP-055. No discrepancies were identified.

Containment Closure Capability for Mitigation of Radioactive

Releases:

Containment closure was maintained and tracked in accordance with

Operation Management Manual procedure OMM-033, Implementation of

Containment Closure, rev. 3. The inspectors reviewed the

procedure and verified that containment penetrations were being

properly controlled to ensure timely closure if required. No

discrepancies were identified.

RCS Temperature Monitoring

The inspectors verified that at least two independent, continuous

indications of RCS temperature representative of core exit

conditions were operable. The operators planned to continuously

monitor the average of the five highest exit thermocouple values

via the licensee's ERFIS computer display in the Control Room.

RCS Level Indication Monitoring

The inspectors verified that at least two independent, continuous

water level indications would be operable during the drain down.

Below 5% in the pressurizer. GP-008 required two RCS local

standpipe and Control Room level transmitters with alarms be in

service. In addition, a continuous local standpipe watch was

required inside containment to verify accurate standpipe

indication. Once level reached -7 inches, the licensee planned to

set-up a camera in the Control Room to monitor the local standpipe

level indication. The inspectors verified that the standpipe

level transmitters had been calibrated via review of calibration

data sheets that were completed on September 4 and 6.

7

RCS Inventory Capability

The inspectors verified that at least two additional means of

adding water inventory to the RCS was required to be available.

PLP-055 required that at least one charging pump and safety

injection (SI) pump with a flowpath from the refueling water

storage tank be available prior to initiating drain down of the

RCS. The licensee planned to have all charging pumps and one SI

pump available for the drain down. The inspectors performed a

partial walkdown of these pumps and their flowpaths on

September 10 and did not note any conditions which impacted

operability.

Emergency Power Availability

PLP-055 required both emergency diesel generators (EDGs) to be

operable during the drain down. Offsite power was provided

through the startup transformer. The inspectors walked down the

EDGs and startup transformer. No adverse material conditions were

identified. The inspectors verified that there was no work

planned in the switchyard during the drain down.

On September 10-12, the inspectors observed operator drain down

activities conducted in accordance with GP-008. An extensive pre-job

briefing of the evolutions was also performed prior to starting the

actual drain down.

During the drain down, a problem was experienced with the pressurizer

cold calibration level instrument LI-462 in that at 22%. level stopped

trending down even though the drain down was still in progress. The

operators secured draining in order to investigate the unexpected

instrument response. A decision was made to valve in the two standpipe

level instruments (normally performed at 5% pressurizer level) to verify

actual level.

When the standpipes were valved in, level indicated 96

inches which corresponded to approximately 10-15 percent pressurizer

level. A work request was written to investigate the level indication

problem with LI-462. The drain down to -7 inches continued with no

further problems encountered.

c. Conclusions

The inspectors concluded that drain down activities were conducted in a

deliberate and controlled manner. A thorough pre-job briefing was

performed prior to the evolution. Important plant parameters such as

RCS level and temperature were closely monitored by the operators.

01.6 Reactor Core Off-Load Activities

a. Inspections Scope (71707)

During September 17-19, the intpectors witnessed portions of fuel off

load activities from the Control Room, containment operating floor, and

8

Spent Fuel Pool Building (SFPB). The inspectors verified that

activities were being performed in accordance with GP-010. Refueling,

rev. 33. and that applicable TSs for conducting refueling activities

were met.

b. Observations and Findings

The inspectors verified that the following TS requirements were met for

conducting refueling activities:

Fuel movement was not initiated prior to 100 hours0.00116 days <br />0.0278 hours <br />1.653439e-4 weeks <br />3.805e-5 months <br /> after shutdown.

At least one airlock door was properly closed and containment

integrity established,

Two source range neutron monitors were continuously being

monitored, each with continuous visual indication in the Control

Room and one audible indication in containment,

At least one Residual Heat Removal Pump was operable.

Refueling cavity level was greater than 272 feet, 2 inches and

average RCS temperature was less than or equal to 140 degrees F,

Direct communication between the Control Room and refueling cavity

manipulator crane was maintained,

Boron concentration was being checked each shift and maintained

above 1950 parts per million, and.

the SFPB ventilation system was operating when handling fuel.

The inspectors also noted that good foreign material exclusion area

(FMEA) controls were setup in containment around the refueling cavity.

Physical barriers and signs were erected to ensure that personnel and

material were positively controlled. In addition, a monitor had been

stationed at the entry point to the FMEA to ensure that personnel

adhered to FMEA controls. While FMEA controls in containment were

considered good, several problems were identified with FMEA controls in

the SFPB. These problems are discussed in Section 01.7.

c. Conclusions

The inspectors determined that fuel off-load activities were performed

in a controlled manner that met or exceeded TS requirements. Good

communications were maintained between the Control Room and fuel

building operators.

9

01.7 Foreign Material Exclusion Area Discrepancies in Spent Fuel Pool

Building

a. Inspection Scope (71707)

While observing fuel off-load activities from the SFPB. the inspectors

noted several FMEA discrepancies. The inspectors reviewed the

licensee's FMEA requirements specified in PLP-047, Foreign Material

Exclusion Area Program, rev. 8, and discussed the discrepancies with

operations management.

b. Observations and Findings

On September 19, the inspectors observed several FMEA problems in the

SFPB. the majority of which resulted from an unauthorized change that

was made to the FMEA boundary. The FMEA boundary had previously been

established around three sides of the Spent Fuel Pool.

On September 17.

fuel handling personnel changed the boundary to exclude the transfer

conveyor control panel from the FMEA. In order to accomplish this, the

FMEA entry point was moved back an entire pool length. However,

personnel failed to update the FMEA material log to remove the material

and items that were logged within the original FMEA boundary.

Additionally, FMEA boundary tape had not been extended to cover either

the new boundary or entry point created by the change. Also, during

review of the FMEA personnel log, the inspectors identified one person

who had not signed out from the previous day.

This item was not

connected to the boundary change problem and appeared to be attributed

to a lack of attention to detail on the part of the person exiting the

FMEA.

The inspectors brought these items to the attention of the licensee.

Immediate corrective actions were implemented to regain control of the

FMEA in the SFPB. The boundary was restored to its original location

and a complete audit of the FMEA material log was completed. The

licensee indicated that several items could not be accounted for,

however, following a visual inspection of the pool, it was determined

that the items had not been introduced into the pool.

Sections 5.1.1 and 5.2.3 of PLP-047 provide the requirements for

establishing FMEA barrier tape and completing the Personnel Log upon

exiting. In addition, PLP-047 assigns responsibility for maintaining

proper FMEA controls to the Supervisor of the employees working in the

FMEA. The inspectors determined that the Shift Supervisors had not been

effective in ensuring that FMEA controls were maintained in the SFPB.

The inspectors noted that similar FMEA procedure discrepancies were

identified in the SFPB during the previous inspection period (See NRC

Inspection Report 50-26/96-10). indicating a continuing trend of

personnel inattention to detail and ineffective supervisory overview of

FMEA requirements.

10

This issue was considered the first of three examples of a violation of

TS 6.5.1.1.1 for failure to follow or inadequate procedures. This item

is identified as Violation (VIO) 50-261/96-11-01:

Failure to Follow or

Inadequate Procedures - Three Examples.

c. Conclusions

The inspectors concluded that personnel failed to follow FMEA procedure

requirements and supervisory overview of FMEA requirements was

ineffective resulting in a loss of FMEA controls inside the SFPB FMEA.

This issue was identified as a violation for failure to follow the

requirements of PLP-047. The deficiencies identified were similar to

previous problems which indicated a continuing trend of insensitivity to

FMEA requirements.

01.8 Operator Assigned to Fire Brigade with Expired Medical Examination

a. Inspection Scope (71707)

The inspectors reviewed the circumstances related to the assignment of

an individual to the Fire Brigade with an expired fire protection

medical examination (physical). The inspectors reviewed the similarity

of this incident to several previous incidents involving expired

physicals for operations personnel and discussed the incident with the

operations and Health Screening personnel.

b. Observations and Findings

On August 15, 1996. the licensee discovered that an Auxiliary Operator

(AO) had been assigned to the Fire Brigade on five previous shifts with

an expired fire protection physical. At the time of discovery, the AO

was in operator retraining class and was not performing shift duties.

On August 20. the AO completed the required physical.

The inspectors

reviewed the medical report for this physical. The individual was

screened for adequate physical and mental conditions required for Fire

Brigade members in accordance with standard 1582 B-3.3-1992 of the

National Fire Protection Association code.

The results of the physical

confirmed that the AO was medically qualified to resume Fire Brigade

activities. The licensee initiated CR 96-01883 to address the expired

physical.

The AOs yearly fire protection physical expired on July 31, 1996. The

inspectors reviewed logs and personnel time sheets for the individual,

as well as other operations personnel on the same shifts between July 31

and August 9, 1996. The inspectors determined that the AO had stood

five shifts during this period and had been assigned to the Fire Brigade

each shift. However, even without reliance on the AO with the expired

physical, the minimum required qualified Fire Brigade complement (five

members) had been available on each of the five shifts.

The licensee's on-site Health Screening organization maintains a

database for tracking and scheduling operator physicals. Physicals are

required to maintain the qualifications for the Fire Brigade (yearly).

respirator certification (18 months), and duties of a licensed operator

(bi-annual). The database contains two important fields that are

delineated as Expiration Date and Scheduled Date. The Expiration Date

field contains the earliest expiration date for any of the three

physicals tracked. The Scheduled Date is two months less than the

Expiration Date, and is used by Health Screening personnel to provide

prior notification to employees that their physical is going to expire.

For the most recent expired physical incident, the Health Screening

organization had previously entered the incorrect date in the Expiration

Date field. Instead of 7/31/96. a date of 10/31/96 was erroneously

entered.

The inspectors reviewed several previous incidents involving similar

occurrences where operations personnel were assigned to duties with

expired physicals. These incidents were documented in CRs 95-01756, 96

00525, and 96-00744.

CR 95-1756 documented the July 10, 1995. expired physicals of two AOs

who were assigned to the Fire Brigade on two consecutive shifts.

Corrective actions included development of the Health Screening database

discussed above which provided notification to the individuals two

months prior their physical expiring.

CR 96-00525 documented a February 1996 Nuclear Assessment Section (NAS)

audit of the Fire Protection Program. During this audit it was

identified that two AOs were assigned to the Fire Brigade with expired

physicals. The root cause of this incident was an erroneous date

entered in the Scheduled Date field. The erroneous date was exactly one

year later than the required schedule date. As a result of this

incident. Health Screening was required to validate that the correct

physical expiration dates had been entered for each of the operators.

The inspectors noted that this review failed to identify the erroneous

physical expiration date for the current incident with the expired AO

Fire Brigade physical.

The erroneous expiration date for the AO had

been entered well before this review was conducted. Other corrective

actions included a March 30. 1996 memo sent from the Operations Manager

to all Fire Brigade qualified personnel reminding them of their

responsibility to maintain their physical requirements current. In

addition, operations initiated the creation of a matrix to track

operator physical expiration dates due to the unreliability of the

Health Screening tracking system.

CR 96-00774 documented a licensed senior reactor operator who stood

seven shifts between March 2-12. 1996, without a current bi-annual

physical as required by 10 CFR 50.55. This incident was the subject of

a Non-Cited Violation (50-261/96-10-01) documented in NRC Inspection

Report 50-261/96-10. The contributing cause of this incident was again,

a data entry error in the Health Screening database. An expiration date

12

of 6/14/96 had been entered instead of 2/24/96 for the operator's NRC

physical. The 6/14/96 date was the expiration date for the operator's

respirator physical. Corrective actions for this incident involved

validation that the NRC physical expiration dates for all "licensed"

operators were correct. Also, a Night Order was issued April 19. 1996,

to reinforce expectations that individuals are responsible for

maintaining their qualifications current. On May 6, 1996, the

operations training matrix was completed and matrix reports were placed

in the Control Room for the operators to review so that they could check

on the status of their medical qualifications.

The licensee's investigation of the current incident determined that the

AO had not reviewed any of the monthly matrix reports placed in the

Control Room beginning in May 1996. The inspectors reviewed the matrix

report which was placed in the Control Room on June 26. 1996. The

portion of the report that provided the Fire Brigade qualifications

showed that the AO's Fire Brigade physical was due on July 31, 1996.

The inspectors considered that the AOs failure to review the report was

a contributing cause to this incident.

10 CFR 50. Appendix B. Criterion XVI. Corrective Action, requires in

part, that measures be established to assure that conditions adverse to

quality are promptly identified and corrected. The inspectors concluded

this issue was a violation of 10 CFR 50. Appendix B. Criterion XVI, in

that the licensee failed to take adequate corrective actions to ensure

that qualifications and conditions for standing watch duties are

maintained current for operations personnel.

This item is identified as

VIO 50-261/96-11-02:

Inadequate Corrective Actions to Prevent Expired

Fire Brigade Medical Physicals.

c. Conclusions

The inspectors concluded that previous corrective actions had not been

effective in ensuring that personnel medical requirements were current

prior to assigning individuals to watch duties. Data entry error in

the licensee's database for tracking medical requirements were not

promptly identified and corrected following initial indications of

problems. In addition, individuals failed to meet expectations for

maintaining the status of their own physical expiration dates. This

issue was identified as a violation of 10 CFR 50. Appendix B. Criterion

XVI.

08

Miscellaneous Operational Issues

08.1 (Closed) Licensee Event Report (LER) 50-261/94-16-01, Reactor Trip Due

to Loss of Load:

On August 2. 1994. with the plant at 100% power the

operators initiated a manual reactor trip when they observed rapidly

decreasing turbine generator. The licensee initiated an events team to

determine the cause of the loss of load. ACR 94-01142 initiated to

document the event and the event team findings.

13

The event team determined that the main turbine governor valves closed

with the unit at full power, resulting in a loss of electrical load. An

intermittent fuse failure in a control circuit that monitors the main

generator output breaker position and closes the governor valve if the

output breakers open with the unit at full load. The licensee

determined that faulty manufacturing caused the fuse failure. An

evaluation of the failed fuse (Bussmann MB010) revealed that it had a

cold solder connection. The licensee concluded that there was no method

available to preclude the installation of fuses with cold soldered

connections. The licensee determined that Limerick had experienced

similar fuse problems with the Bussmann KTN-10 and testing results

yielded a 30% failure rate. Bussman redesigned the fuse to provide a

larger base to make the soldered connection. The redesigned fuse

appears to have solved the manufacturing problem.

The inspectors reviewed the completed ACR 94-01142. including the event

team report. The licensee's actions appear to be adequate and this item

is closed.

II. Maintenance

M1

Conduct of Maintenance

M1.1 Refueling Outage Contractor Maintenance Discrepancies

a. Inspection Scope (62707)

The inspectors reviewed the circumstances associated with two outage

related contractor field work errors.

b. Observations and Findings

Failure to Follow Modification Instructions

On September 16, unit was in Cold Shutdown with the refueling

cavity filled and control rod unlatching ongoing. Two contracted

electrical technicians were performing cable replacement

activities associated with modification Engineering Service

Request (ESR) 95-00764. The technicians received turnover from

night shift personnel that the cable replacement associated with

valve SI-866A was ready to be performed. SI-866A is the RCS Loop

3 SI Pump Discharge Hot Leg Injection Valve. The valve was

closed, but was being maintained available for core inventory

addition in accordance with the risk management procedure PLP-055.

Due to a shift turnover communication error. the technicians

believed that the valve had already been tagged out of service

(i.e., permission granted from operations to perform the work and

clearance tag obtained). Valve tagout was required in accordance

with steps 16.1 through 16.4 of ESR 95-00764. The technicians

failed to review the "master" copy of ESR 95-00764 which would

have alerted them to the fact That these actions had not been

signed off and the valve was still energized. The technicians

14

proceeded to cut the valve cables in accordance with step 16.5 of

ESR 95-00764. After cutting the cables, the technicians noticed

electrical arcing and realized that the cable had been energized.

Immediately following the incident, the licensee stopped all work

on ESR 95-00764 to begin an investigation. Later, all electrical

work being performed by the contractor was stopped and a "stand

down" was performed. The stand down emphasized proper shift

turnover communications and management expectations that the

"master" modification copy be reviewed prior to starting work each

shift.

This issue was identified as the second of three examples of a

violation of TS 6.5.1.1.1 for failure to follow procedures. This

item is identified as VIO 50-261/96-11-01:

Failure to Follow or

Inadequate Procedures -

Three Examples

Partial Valve Disassembly Error

On September 18, an engineer monitoring the progress of Boric Acid

(BA) pipe replacement work observed a mechanical contractor worker

beginning to disassemble valve MOV-350, the charging pump suction

supply from the BA Blender. The engineer noted that red clearance

tags were hung on the valve and recognized that it was being

maintained part of the clearance boundary for integrity of the

cold leg injection flowpath in accordance with PLP-055. Breaching

this boundary would have rendered this flowpath inoperable. The

engineer directed the worker to stop work. At this time, one body

to bonnet stud had been removed and the nuts to another stud had

been loosened. The valve was immediately restored to its original

condition.

The inspectors determined that work had not yet progressed to the

point of breaching the actual integrity of the boundary. The

licensee's preliminary investigations attributed the cause of the

incident to worker confusion of his work assignment,

miscommunication between the worker and his supervisor, and

inattention to detail.

As a result of these significant and other minor outage related work

incidents, licensee management ordered a site-wide "Work Stand-Down."

The stand-downs were conducted on September 18-19 for all work groups.

The inspectors attended the operations stand-down conducted by the

Control Room Shift Supervisor with all shift operations personnel. At

this meeting. each of the specific work related problems were reviewed

including the cause and lessons learned. Proper work practices were re

emphasized regarding communications, attention to detail, and use of

STAR (Stop. Think. Act, and Review).

The inspectors judged the effectiveness of this stand-down was good. At

the end of the report period, no other significant outage-related work

error were identified.

15

c. Conclusions

The second example of a violation for failure to follow procedures was

identified when a contractor cut the power cable to valve SI-866A

without first obtaining operations authorization or obtaining a

clearance for the work. Another significant contractor work control

error involved the unauthorized partial disassembly of a boundary valve

for maintaining integrity of the charging pump suction line. The

licensee's stand-down to reemphasize work control expectations and

requirements following these incidents was considered effective in

preventing further serious problems.

M1.2 Equipment Repetitive Failure Program

a. Inspection Scope (62700

The inspectors reviewed plant documentation to identify equipment that

had repetitive failures. The repetitive failures were examined to

determine the root cause of maintenance problems and the corrective

action implemented by the licensee. The plant equipment "Repetitive

Failure List" was reviewed to identify the components that had recurring

corrective maintenance problems identified during 1994, 1995, and 1996.

The Maintenance Department's monthly report "Maintenance Inappropriate

Acts" for July 1996 was examined to review the licensee's self

assessment in this area. Several Condition Reports (deficiency reports)

were reviewed to determine the adequacy of Engineering evaluations in

support of maintenance. In addition, the plants "Top Ten" Equipment

Issues List was reviewed to determine if the licensee was addressing and

implementing corrective action for components that had recurring

maintenance problems.

b. Observations and Findings

The inspectors reviewed 94 work order (WO/JO) for 33 components and

systems listed in the "Repetitive Failure List". All the WO/JO reviewed

were for corrective maintenance that was performed within six months of

the previous work. In most cases, the repetitive work was performed

within months of the previous work. The systems with the most

repetitive work were Instrument air: HVAC (heating, ventilation, and air

conditioning) for the control room: and the Hypochlorite system. The

components with the most repetitive failures were instruments (DP

transmitters), air filter regulators, leaking valves, gaskets and seals,

battery chargers, and electronic instrument modules. The inspectors

identified that most of the repetitive failures were caused by aging of

the equipment such as the Hagan instrument modules or inadequate design

for the installation of the DP transmitters. Repetitive failures for

leaks in valve packing and gaskets and seals leaks in pumps were not

considered abnormal.

The components with the highest rework such as

electronic instrument modules, air compressors. filter regulators, air

condition equipment, and the Hypochlorite valves and piping have been or

are being replaced or upgraded. The licensee has an ongoing program to

16

replace the capacitors in the existing Hagan instrument modules. The

Hagan modules are also being replaced with a new type.

The licensee had identified most of the repetitive failures and was in

the process of implementing appropriate corrective action. These

repetitive failures were placed on the "Top Ten" Equipment Issues List

or identified in the monthly "Maintenance Inappropriate Acts" Report.

Both the Hypochlorite and Instrument Air systems were on the "Top Ten

list for corrective action. Components listed on the "Top Ten" included

DP transmitters and the Hagan electronic instrument modules which have

caused most of the repetitive failures in the instrument area.

The "Maintenance Inappropriate Acts" Report covered two areas, 1)

maintenance due to personnel errors and 2) inappropriate acts involving

rework. Both areas were self assessments to identify and correct

maintenance repetitive problems. Both areas had implemented Conditions

Reports (deficiencies) that were addressed by System Engineering in

support of maintenance. The inspectors reviewed seven Condition Reports

that were used for evaluations of personnel errors and thirteen

Conditions reports that were used for evaluations for rework caused of

by inappropriate acts.

Personnel errors were mistakes made during the

implementation of specified work.

Inappropriate acts were someone

performing something not specified on a work order or something

maintenance had no control over such as defective parts or wrong vendor

information. Some of these rework items for 1996 included items such as

five damaged components, three improper designs, three miss adjustments,

six inadequate decisions, and five defective replacement parts.

c. Conclusion

The inspectors concluded that Maintenance Department, with Engineering

support, was in the process of identifying repetitive failures. In

addition, several effective programs such as the "Top Ten List", the

"Repetitive WO/JO List", the "Equipment Failure List", and the

"Maintenance Inappropriate Acts" have been initiated by the licensee to

identify and minimize repetitive failures. The inspectors concluded the

licensee has effectively identified repetitive failures and was in the

process of implementing appropriate corrective action.

M8

Miscellaneous Maintenance Issues (92902)

M8.1

(Closed) LER 50-261/93-16-00, Ventilation System Outside Design Basis

Due to Positive Pressure Condition:

During the performance of

Operations Surveillance Test OST-411, Emergency Diesel Generator "B"

(Twenty Four Hour Load Test), licensee personnel questioned the airflow

from the Emergency Diesel Generator (EDG) "B" room to the Reactor

Auxiliary Building (RAB) hallway. Investigation revealed that the EDG

room recirculation damper was not opening as designed for the ambient

air temperature conditions. The EDG room recirculation dampers were

designed to change operating modes at an ambient air temperature of 55

degrees F (Winter and Summer modes). The EDG Exhaust Fan operates at

low speed and the recirculation damper opens when the ambient

17

temperature is below 55 F. allowing the warm air to recirculate back to

the EDG room. The EDG Exhaust Fan switches to fast speed and the Air

Recirculation Return Damper closes when in the summer mode. The outside

ambient temperature during the performance was less than 55 degrees.

The as found configuration resulted in the RAB pressure becoming

positive. The design of the RAB Ventilation System provides positive

control of the potentially contaminated RAB environment.

Investigation

by the licensee determined that a damper solenoid valve was miswired

which resulted in the solenoid not receiving an actuation signal.

This event resulted in the NRC issuing Unresolved Item (URI) 50-261/93

11-04. The URI was closed in Inspection Report 50-261/93-19. The

closure of the URI also closes this item.

M8.2 (Closed) LER 50-261/93-21-00, Technical Specification Violation Due to

Missed Channel Functional Test:

On November 30, 1993, a licensee

technician identified that the plant vent monitor (RMS-14) had not had

its technical specification required quarterly functional test within

the specified time period. The quarterly time limit for the channel

functional test was exceeded by nine days. The due date for the test

was October 29, 1993. However the plant was in an outage and the

licensee decided to reschedule the test until after plant restart.

Technical specifications allow the functional test period to be exceeded

by 25 percent, thus making its overdue date November 21, 1993. The

startup was delayed and the E&RC supervisor did not recognize that the

functional test had to be performed before startup.

On November 30, 1993, the licensee successfully performed the plant vent

channel functional test. There was no safety significance to the late

channel functional test. The licensee instituted a system in which all

surveillance/functional tests are scheduled and tracked in a single

system. The licensee addresses late surveillances at their morning

management meetings which the inspectors observe. There have been no

additional examples of overdue surveillances since the licensee

implemented their corrective actions. The inspectors have concluded

that the licensees corrective action was adequate and this item is

closed.

M8.3 (Closed) Inspector Followup Item (IFI) 50-261/94-028-03. Follow

Licensee's Activities to Enhance The On-Line Maintenance Scheduling

Process: The inspectors concluded that the licensee did not require

formal evaluations of increased risk due to on-line maintenance. The

licensee has incorporated a matrix which was based on an evaluation the

risk of performing maintenance on various combinations of two systems.

The inspectors reviewed Plant Program Procedure, PLP-056. Work Control

Process, Revision 11.

Section 3.3 states that the matrixes only apply

for combinations of one or two system trains at a time. Further

analysis is required if three or more system trains need to be

unavailable at the same time. Section 5.6.k states that Plant General

18

Manager approval is required for combinations not allowed by the matrix

or not otherwise evaluated as acceptable.

The inspectors have concluded that the licensee's program does require a

formal evaluation of risk significant maintenance and this item is

closed.

III. Engineering

El

Conduct of Engineering

E1.1 Main Steam Isolation Valve Failure to Close

a. Inspection Scope (37551)

The inspectors reviewed licensee investigations of the A Main Steam

Isolation Valve (MSIV) failure to close during unit shutdown. The

inspectors observed valve troubleshooting, visually inspected the valve

internals, and discussed with engineering their findings regarding the

failure.

b. Observations and Findings

On September 9. at 1:06 a.m., the operators attempted to close all three

MSIVs. At the time, unit cooldown was in progress and the RCS was at

2210 F. Repeated attempts to close the A MSIV from the control board

were unsuccessful.

The operators continued the cooldown reaching Cold

Shutdown conditions (2000 F) at 2:50 a.m. Initial licensee

troubleshooting results indicated proper functioning of the MSIV's air

operated solenoid valves, actuator, and packing clearances. Following

these activities, a more exhaustive troubleshooting plan was developed

by engineering for disassembling the valve.

Between September 9-10, the inspectors witnessed portions of the

licensee's disassembly of the valve to determine why it would not close.

The inspectors noted that activities were well controlled and

coordinated by engineering personnel to ensure that root cause data was

obtained. No evidence of problems were identified during removal of the

valve packing and actuator. When the valve bonnet was removed, the

licensee discovered that the outer edge of the valve disk was in contact

with the valve body at two locations. This caused the disk to wedge

between the disk hinge pin and the two points of contact on the valve

body. With only a slight tap on the top of the disk, it slammed closed,

indicating that it was not being held tightly.

The inspectors met with licensee engineers on several occasions to

discuss their investigations and results. The licensee determined that

the disk failed to close because it became thermally bound inside the

valve body. The licensee believed that the outer edge of the disk may

have been in slight contact with the inside valve body when the valve

was open during power operations. Following plant shutdown, the disk

and valve body cooled at different rates, resulting in the disk becoming

thermally bound.

19

The licensee believed that the unexpected contact between the disk and

valve body was attributed to a combination of effects. In 1978. a

heavier disk was installed to address potential dynamic concerns with

the closing forces. As a result, this may have changed the closeness of

the disk in relation to the top of the valve body. Additionally, in

1993, the valve spindle was replaced. The new spindle was slight

shorter than the old. Based on the valve design, a shorter spindle

would also have an effect of raising the disk inside the valve body.

The licensee believed that the combination of these changes caused the

disk to slightly contact the edge of the valve body. The inspectors

reviewed the licensee's evaluations and determined that they had

adequately determined the reason for the valve failure to close.

The licensee determined that this condition would not have caused a

problem at normal operating conditions since the disk and valve body

would have been at similar temperatures. Associated with this part of

the investigation, the licensee hired a contractor to perform an

independent engineering evaluation of the condition. This evaluation

was performed by Kalsi Engineering Inc. The inspectors reviewed the

preliminary report from the contractor which concurred with the

licensee's conclusions. The inspectors concluded that the licensee had

adequately resolved whether the valve was capable of fulfilling its

required safety function had an isolation signal been generated.

The inspectors reviewed the licensee's corrective actions to eliminate

the possibility of recurrence of the valve sticking in the open

position. The licensee planned to modify the A MSIV disk by grinding

the outer edge to provide greater clearance between the valve body and

disk to eliminate the chance of thermal binding. In addition, a longer

replacement valve spindle was to be installed, which would lower the

position of the disk in the valve body. These actions were going to be

performed prior to plant startup. The inspectors determined that these

actions were adequate to prevent recurrence. Similar disk to valve body

clearance checks were planned for the other two MSIVs. In addition,

testing will be performed on all MSIVs prior to startup.

c. Conclusions

The inspectors concluded the licensee had conducted a thorough

investigation and analysis of the valve failure. Investigation results

supported the licensee's determination that the valve would have closed

at operating conditions. Planned licensee actions for correcting the

disk to valve body interference problem in the A MSIV were determined to

be adequate.

E7

Quality Assurance in Engineering Activities

E7.1 Special UFSAR Review

A recent discovery of a licensee operating their facility in a manner

contrary to the Updated Final Safety Analysis Report (UFSAR) description

highlighted the need for a special focused review that compares plant

20

practices, procedures and/or parameters to the UFSAR descriptions.

While performing the inspection discussed in this report, the inspectors

reviewed selected portions of the UFSAR that related to the areas

inspected. The inspectors verified that for the select portions of the

UFSAR reviewed, the UFSAR wording was consistent with the observed plant

practices, procedures and/or parameters.

E8

Miscellaneous Engineering Issues (37551 and 92903)

E8.1

(Closed) IFI 50-261/95-20-01, Justification of Time Required to

Establish Alternate SI Pump Thrust Bearing Cooling: The licensee had

taken credit in their plant specific analysis (PSA) for establishing

alternate cooling to the Safety Injection (SI) pump thrust bearings to

mitigate the consequences of a total loss of service water. The

licensee stated this action could be accomplished within 45 minutes;

however, there was no justification to support this 45 minute time

allowance. The inspectors reviewed the licensee's PSA for a total loss

of service water and found that the analysis determined that core

uncovery would occur within 2.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />. The inspectors determined that

this 2.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> would be sufficiently bounding to support the 45 minute

allowance to establishing alternate cooling to the SI pump thrust

bearings.

The inspectors reviewed the assumptions made in the PSA to support the

2.5 hour5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br /> conclusion. One of the assumptions was that reactor coolant

pumps (RCPs) were tripped within one minute after a loss of all cooling:

either from seal injection or by the thermal barrier. The inspectors

reviewed the applicable plant procedures to determine if the one minute

assumption in the PSA was supported by plant procedures. Although

specific guidance on the one minute RCP trip was not available, further

discussions with the licensee indicated that the operators would enter

the Emergency Operating Procedure (EOP) network first due to inability

to provide cooling to turbine building loads resulting in a forced

manual reactor trip. The necessary guidance to trip the RCPs was

contained in the EOPs.

Furthermore, the licensee stated that tripping

the RCPs was a simplifying assumption and the smallest time step allowed

was one minute. Because of the large margin in the time to core

uncovery (2.5 hours5.787037e-5 days <br />0.00139 hours <br />8.267196e-6 weeks <br />1.9025e-6 months <br />), the inspectors determined the allowance of 45

minutes to establish alternate cooling to the SI pump thrust bearings

was adequately supported.

E8.2 (Closed) IFI 50-261/95-20-02, Evaluation of Air Operated Valves "Smart

Failures":

This issue addressed the potential for non-conservative

valve positioning resulting from failure of non-safety related

controllers and positioners rather than a complete loss as addressed in

Generic Letter (GL) 88-14. The licensee provided documentation that a

safety-related positioner was downstream of any non-safety related

controllers or positioners. This ensured the valve positioned correctly

even in the event of a failure of a non-safety related device. The

presence of this safety-related positioner adequately addressed the

concern. Furthermore, the licensee was not required by GL 88-14 to

analyze for such failures: only for a loss of instrument air.

21

IV. Plant Support

R1

Radiological Protection and Chemistry Controls (71750)

R1.1 Tours of the Radiological Control Area

a. Inspection Scope (71750)

The inspectors periodically toured the radiological control area (RCA)

during the inspection period. The inspectors reviewed and discussed

"hot particle" events and reviewed selected skin dose evaluations

associated with the current refueling outage.

b. Observations and Findings

Radiological control practices were observed and discussed with

radiological control personnel including RCA entry and exit, survey

postings. locked high radiation areas, and radiological area material

conditions.

Locked high radiation area controls were verified to be implemented in

accordance with TS requirements. Posting of radioactive waste

(radwaste) storage areas were proper and containers holding radioactive

waste, materials or contaminated equipment were labeled adequately.

Within the RCA, general housekeeping was considered acceptable.

The inspectors reviewed four skin dose assessments associated with "hot

particle" contaminations during the current outage. The inspector

verified that the assessments were conducted in accordance with

corporate procedure DOS-NGGC-005, Skin Dose from Contamination, Rev. 0,

dated June 7. 1996. For the worker assessments reviewed, a maximum skin

dose of 1880 millirem (mrem) was calculated.

c. Conclusions

Posting and labeling of radiation areas or containers of radioactive

material were conducted in accordance with 10 Part 20 requirements.

Licensee programs to assess "hot particle" skin exposures during the

current outage were adequate.

R1.2 Release of Worker from Site with Clothing Contamination

a. Inspection Scope (83750)

The inspectors reviewed the licensee evaluation and corrective actions

documented in Condition Report (CR) 96-01983 addressing an August 27,

1996 personal contamination event resulting in a subsequent release of a

worker with slightly contaminated clothing from the site were reviewed

and discussed in detail.

22

b. Observations and Findings

Licensee CR 96-01983 documented an August 27, 1996, contamination event

involving several individuals and which subsequently resulted in the

release of one individual from the site whose clothing was contaminated

slightly above background. The evaluation identified that on August 27,

1996, three painters were contaminated during preparation (needle gun

paint removal) of the Spent Fuel Pool deck area floor in preparation for

painting. Surveys of adjacent areas, and loose contamination and

airborne surveys conducted during the job evolution did not indicate any

significant contamination for the area. However, upon exiting the

Radiologically Controlled Area (RCA) all the painters alarmed the

personnel contamination monitors. Following decontamination activities,

two of the painters did not clear the monitors nor meet frisker limits,

i.e. having contamination greater than 100 corrected counts per minute

(ccpm) above background. The clothes of the two painters were

confiscated. For the third painter, a senior RC technician conducted a

frisk which identified contamination levels of approximately 20-40 ccpm.

The RC technician allowed the individual to exit the RCA with the

identified counts erroneously attributed to noble gas contamination.

Upon leaving the restricted area, the same painter alarmed the portal

detectors corresponding to the right foot and leg.

The same RC

technician responded and allowed the individual to leave the restricted

area without a required frisk being conducted based on the individual

not having re-entered the RCA. The next day, all painters involved in

the needle gun activities were sent for whole body analysis. Upon

exiting the restricted area, the same painter who alarmed the portal

monitor the previous night, re-alarmed the restricted area portal

monitors. Followup surveys conducted in the low radiation background of

the restricted area boundary indicated contamination, approximately 120

ccpm, on the painter's shoes. Further, followup whole body analyses

identified an intake of Cesium-137 resulting in Committed Effective Dose

Equivalent of approximately 1 mrem to each individual.

TS 6.11 requires, in part, procedures for radiation protection to be

prepared consistent with the requirements of 10 CFR Part 20 and to be

approved, maintained and adhered to for all operations involving

personnel radiation exposure. From review of procedure and survey

guidance the licensee identified the following examples of failure to

follow procedures which contributed directly to release of the

contaminated clothing from the site:

The lead technician improperly identified the contamination as

noble gas contrary to guidelines for radon progeny discrimination

detailed in Health Physics Procedure-005. Control of Personnel

Decontamination Techniques. Rev. 31 and Survey Instrument

Calibration Procedure -011, Calibration and Operation of the NE

Technology Delta 3 Portable Ratemeter, Rev. 1.

23

The lead technician failed to follow Plant Program Procedure-031.

Contamination Monitoring Program for Personnel/Personal Effects,

Rev. 16, in that, a frisk was not conducted after the individual

alarmed the restricted area portal monitor.

In addition, the licensee's evaluation identified a procedure weakness

in that fixed-contamination surveys were not conducted prior to

initiating needle gun activities although the exact radiological

contamination history was unknown and repainting had been conducted for

the area. Licensee corrective actions included immediate notification

of RC technicians regarding the sequence of events and lessons learned,

proposed revisions to procedures for performing fixed contamination

surveys prior to conducting abrasive work, evaluation of training needs

for the staff, improve documentation by RC personnel regarding

unusual/abnormal conditions and evaluation of techniques for abrasive

removal of paint to reduce radiological hazards. The inspectors

identified the failure to follow procedures as non-cited violation (NCV)

50-261/96-11-03: Failure to follow procedures for personnel

contamination surveys, consistent with Section IV of the NRC Enforcement

Policy.

c. Conclusions

An NCV was identified for failure to follow procedures for personal

contamination control activities in accordance with TS 6.11.

R1.3 Radioactive Waste and Material Transportation Activities

a. Inspection Scope (86750. T12515/133)

The inspectors reviewed RC program activities associated with packaging

and shipping of radioactive material and waste to either vendor

processing facilities or directly to a licensed burial facility. The

review included evaluation of shipping and packaging activities for the

following radioactive material shipments.

A November 17, 1995, Reportable Quantity (RQ) Radioactive

Material, Low Specific Activity. N.O.S. 7, UN2912.

A December 29. 1995, RQ Radioactive Material. Low Specific

Activity, N.O.S. 7, UN2912,

An August 12, 1996. RQ. Radioactive Material. Fissile, N.O.S. 7,

UN2918,

A September 19, 1996 Radioactive Material Shipment, Low Specific

Activity, N.O.S. 7, UN2912,

The inspectors verified and evaluated implementation of revised

49 CFR Parts 100-179 and 10 CFR Part 71 regulations. In addition, the

inspectors evaluated licensee response to a simulated accident scenario

involving a September 18. 1996 radioactive material shipment.

24

b. Observations

Licensee shipping paper documentation met the applicable regulatory

requirements. One potential weakness for management consideration was

restricted visibility of the emergency phone number on some shipping

papers reviewed. The inspectors verified that licensee was a registered

user of the shipping casks and that the appropriate Certificates of

Compliance were maintained at the facility and used to develop the

licensee procedures used to conduct the reviewed shipping activities.

In addition, the inspectors verified that changes to 49 CFR Parts 100

179 and 10 CFR Part 71 regulations were implemented as required.

The response to the simulated emergency scenario was satisfactory,

requiring approximately 15 to 18 minutes for operators in the control

room to provide all the required information to the inspectors.

Licensee representatives stated that the observed response time resulted

from the operators contacting onsite RC supervision prior to completing

a full response to the inspector. Further, operators were trained to

respond directly to an transportation accident event, as necessary. The

inspectors noted that licensee evaluation of this area was continuing

and that supplemental training accident scenarios would focus on

increasing the operators' timeliness in providing the required emergency

response information.

c. Conclusions

Transportation and packaging activities for radioactive waste or

material shipments met 10 CFR 71.5 and 49 CFR 100-179 requirements. The

licensee was implementing, as required, revised Department of

Transportation (DOT) guidance.

R2

Status of Radiation Protection and Chemistry Equipment and Facilities

R2.1 Radiation Monitor System Installation and Operation

a. Inspection Scope (84750)

The inspectors reviewed and evaluated the adequacy of installed process

and effluent Radiation Monitoring System (RMS) detectors, particulate

and iodine samplers, electronics, sampling lines and flow meters, as

applicable, to meet UFSAR commitments and to implement Offsite Dose

Calculation Manual (ODCM) and 10 CFR Part 20 requirements. The

evaluation included, as applicable. RMS equipment walk-downs with

comparisons against configuration control documents, design change

notices and vendor design specifications. Further, the installed sample

line bend radii and piping specifications were evaluated against

recommendations detailed in American National Standards Institute (ANSI)

N13.1-1969, American National Standard Guide to Sampling Airborne

Radioactive Materials in Nuclear Facilities. General comparisons were

made between radiation monitor local and remote readout data, where

possible.

25

The following RMS samplers or detectors (Rs), and associated equipment

were included in the review: Spent Fuel Pool area (R-5): Drumming Room

area (R-8); Failed Fuel process (R-9); Containment Atmosphere

particulate (R-11)

and gas (R-12); Plant vent gas, particulate and

iodine (R-14); Service Water header (R-16); Component Cooling water

process (R-17): Liquid Waste effluent discharge (R-18); Fuel Handling

Building lower (R-20) and upper (R-21) exhaust; Steam Line discharge (R

31 A. B & C); and Containment High Range Monitor (R-32 A&B).

b. Observations and Findings

For the RMS equipment reviewed, no significant issues regarding design

specifications, installed system equipment and sample line

configurations, and operating parameters were identified. Housekeeping

practices associated with RMS equipment skids, cabinets and general

areas were appropriate.

No significant differences were identified for comparisons of data

supplied at local and remote, e.g., Main Control Room. RMS readouts.

Sample flow rates were within limits specified within vendor manuals.

c. Conclusions

The RMS equipment was designed, installed, operated and maintained

appropriately.

R2.2 Radiation Monitor System Calibrations

a. Inspection Scope (84750)

Approved guidance and resultant data for selected RMS detector

calibrations were reviewed and discussed. For each detector reviewed,

source calibration Environmental and Radiation Control (E&RC)

Surveillance Test Procedure (STP) packages for the previous two

surveillances conducted prior to the onsite inspection were reviewed,

evaluated and discussed with licensee representatives. The following

RMS detectors and associated electronics were included in the review:

Main Control Room area (R-1): Spent Fuel Storage Pool area (R-5):

Containment Atmosphere particulate (R-11)

and gas (R-12): and

Containment High Range Monitor (R-32B).

The RMS source calibration guidance and results were evaluated against

applicable sections of the UFSAR, Technical Specification (TS) and ODCM

requirements. In addition. STP guidance for the R-32 monitor was

compared against special calibration requirements specified in

NUREG 0737, Clarification of Three Mile Island (TMI) Action Plan

Requirements. Table II.F.1-3 Containment High Range Monitors (CHRMs).

b. Observations and Findings

From the RMS detector source calibration reviewed, no concerns nor

issues were identified. Further, the inspectors verified completion of

26

in situ special calibrations by electronic signal for the CHRMS in

accordance with TMI Action Item II.F.I-3 specifications. No significant

trends in the calibration data were observed and all surveillances were

conducted at the required frequencies. Traceability of calibration

sources and calibrator equipment to National Institute of Standards and

Technology (NIST) was demonstrated.

c. Conclusions

The RMS detector source calibrations were technically adequate,

conducted at required frequencies and results were within established

limits.

R5

Staff Training and Qualifications in Radiation Protection and Chemistry

R5.1 Training of RC Staff on Transportation Requirements

a. Inspection Scope (86750. TI 2515/133)

The training provided to RC staff to meet the requirements of

49 CFR Part 172 Subpart H were reviewed and discussed with licensee

representatives. Further, training details provided to staff regarding

implementation of recent Department of Transportation (DOT) changes to

49 CFR Parts 100-179 were evaluated.

From discussion with applicable RC staff members, the inspector

evaluated the training effectiveness regarding recent DOT changes

implemented for 49 CFR Parts 100-179.

b. Observations and Findings

Review of training records verified that RC staff members involved in

handling and packaging of radioactive materials were receiving hazardous

material (hazmat) training within the required frequencies. From review

of training material presented to staff in March 1996, the inspectors

verified that recent DOT changes to shipping and packaging requirements

were covered in the course material.

From discussion of shipping

procedures and shipping papers, the inspectors determined that

responsible licensee representatives were knowledgeable of the recent

DOT changes.

c. Conclusions

Hazmat training provided to personnel handling radioactive materials was

conducted at the appropriate frequency. and included recent changes to

DOT regulations. The training provided was effective.

27

R7

Quality Assurance in Radiation Protection and Chemistry Activities

R7.1 Radiological Measurement Quality Control

a. Inspection Scope (84750)

The inspectors reviewed implementation of the counting room quality

control (QC) activities to meet the intent of Regulatory Guide (RG)

4.15. Quality Assurance for Radiological Monitoring Programs (Normal

Operations) - Effluent Streams and the Environment. Specifically, the

results of the following cross-check radiological analyses were reviewed

and discussed with cognizant licensee representatives:

1995 quarterly cross-check analysis results for strontium (Sr)-89.

Sr-90, and iron (Fe)-55 Vendor Analyses

1995 quarterly and 1996 first quarter cross-check analysis results

for gamma-spectroscopy analyses

Selected 1996 Daily Gamma Spectroscopy System Performance Data.

.The use of correction factors, as applicable, for RMS sample line

particle deposition and iodine plate-out were reviewed and discussed.

The review included calculations and actual test data used to evaluate

particle deposition and iodine plate-out in RMS sample lines. Finally,

the licensee evaluation of design limitations for the.plant vent gaseous

effluent monitor under accident conditions as identified in NRC

Information Notice 86-30. was reviewed and discussed.

b. Observations and Findings

No significant concerns nor negative trends were identified from review

of the counting room gamma-spectroscopy QC performance data. In

addition, no issues regarding inter-laboratory cross-check analyses were

noted.

From discussions with licensee representatives, the inspectors were

informed that airborne effluent measurement data did not include

correction factors for iodine plate-out nor for particulate deposition

in sample lines. The inspectors noted that particulate and iodine

radionuclides are routinely monitored by the Containment Atmosphere

(R-11) and the Plant vent (R-14) sampling systems. Licensee

representatives provided a March 1987 study which compared results from

a particulate filter and charcoal cartridge on the R-11 RMS to a

containment grab sample. For the particulate radionuclides, the ratio

of R-11 sampler to Containment Volume (C-11/CV) grab sample values

ranged from .8 to 1.4. For the iodine radionuclides, the C-11/CV ratios

ranged from 1.10 to 1.13. For the R-14 monitor, a preliminary

evaluation of changes to the system indicated that the monitor upgrade

would not affect sample line deposition with approximately 100 percent

of particulates transmitted to the sample collector. However, no

calculations were provided with the evaluation nor were any estimates of

28

iodine plate-out provided. Subsequent evaluation of sample line

deposition using Deposition Software for Characterizing Aerosol Particle

deposition in Sampling Lines. Revision 2. calculated a transmission

factor of approximately 99.5 percent. The inspectors noted either

calculations or test studies evaluating RMS sample line particulate

deposition and iodine plate-out needed to be formally documented and

approved.

In addition, the licensee was unable to provide data prior to the end of

the onsite inspection, regarding qualifications of the R-14 electronic

equipment for doses expected during accident conditions. A preliminary

calculation indicated that expected doses, approximately 850 rads. would

be less than the 1000 rads operating limit specified by the vendor.

The inspectors informed licensee representatives that calculations

ensuring the R-14 monitor was qualified to expected doses during

accident conditions, as well as data associated with evaluation of

sample line particulate deposition and iodine plate-out. would be

reviewed during subsequent inspections.

c. Conclusions

Gamma spectroscopy and inter-laboratory cross check QC activities were

implemented appropriately and met the intent of RG 4.15. A need to

review documentation associated with sample line particulate and iodine

plate-out calculations and qualification of the R-14 monitor to expected

doses during accident conditions was identified as IFI 50-261/96-11-04.

R7.2 Licensee Self-Assessment Activities

a. Inspection Scope (84750, 86750)

During the inspection period, the following audit reports regarding

Chemistry, RC: and Radioactive Waste (Radwaste) processing, packaging

and transportation program activities required by TS, 10 CFR Part 20,

and 10 CFR Part 71 were reviewed and discussed with licensee

representatives.

R-ERC-94-02, Environmental and Radiation Control Assessment, dated

January 10, 1995

R-ERC-95-01, Environmental and Radiation Control Assessment, dated

January 05, 1996

In addition, the experience of the individuals conducting audits of the

subject E&RC program areas was reviewed and discussed.

b. Observations and Findings

The audits met TS required frequencies and addressed ODCM. effluent,

Chemistry, RC, radwaste and transportation program guidance and

implementation. Both compliance-based and performance-based strengths,

29

issues, weaknesses and recommendations were documented. The audits

included review and followup of previously identified items.

From discussions with licensee management, the inspectors determined

that auditor teams included experienced individuals from outside of the

H.B. Robinson facility.

c. Conclusions

Audits for the E&RC program activities were thorough and comprehensive,

and met TS, 10 CFR Part 20, and 10 CFR Part 71 requirements.

P2

Status of Emergency Preparedness Facilities, Equipment, and Resources

P2.1 Testing of Public Warning System Following Hurricane

a. Inspection Scope (71750)

The inspectors reviewed the licensee's actions to test the Public

Warning System sirens located in the surrounding counties following

Hurricane Fran.

b. Observations and Findings

On September 6, the licensee conducted a silent test of the Public

Warning System sirens to ensure that there was no damage as a result of

the strong storm winds from Hurricane Fran.

This test involved sending a test actuation signal to each of the sirens

from the primary activation point. Receipt of the signal, and therefore

affirmation that the sirens would actuate, was confirmed by reading a

local counter at each of the sirens.

During this test, the licensee identified that a significant number of

sirens in Darlington County did not receive the test signal.

As a

result of the potentially inoperable siren conditions, the licensee

implemented their offsite emergency management procedures for backup

public warning in the affected areas. Also, in accordance with 10 CFR

50.72(b)(1)(v), the licensee provided a 4-hour NRC notification due to

meeting the criteria for a major loss of offsite communication

capability. Later that same day, another silent test was conducted from

the alternate activation location. The results of this test confirmed

that all but one siren was operating properly.

Subsequent licensee investigations determined that the cause of the

original failures was a malfunctioning tone encoder used to transmit the

test signal from the primary activation location. In that the alternate

activation equipment had been operable, the sirens could have been

actuated during the time that the primary tone encoded equipment had

failed. The primary tone encoder was later replaced and an acceptable

silent test was performed to demonstrate siren operability.

30

c. Conclusions

The inspectors concluded that licensee actions to test and address

potential problems with the Public Warning System following the

aftermath of Hurricane Fran were adequate.

P3

Emergency Preparedness Procedures and Documentation

P3.1 Discrepancies in On-shift Dose Assessment Procedure

a. Inspection Scope (71750)

The inspectors reviewed the licensee's capability to conduct on-shift

dose assessments during accident situations. This included a review of

emergency procedures and discussions with operators, emergency

preparedness (EP), and computer support personnel.

b. Observations and Findings

10 CFR 50.47 requires that licensees have the capability to perform dose

assessments at all times in order to support emergency response efforts

during accident situations involving actual or potential releases of

radioactive material.

This requirement makes it necessary to have

personnel on-shift who are capable of performing dose assessment

calculations.

The inspectors reviewed emergency procedure EPRAD-03, Dose Projections.

rev. 0. The Control Room operators are responsible for performing dose

projections until the Dose Projection Team, who are part of the

Emergency Response organization, arrive onsite and are prepared to

provide this function. The procedure provided instructions for

accessing a dose calculation computer program called "HBRDOSE" via

several different options. The first and primary option included

accessing the program via an Emergency Response Facility Information

System (ERFIS) terminal computer. If the ERFIS link was operational,

the system would retrieve the input data automatically. If this link

was not operational, the operators would be required to enter the input

data manually. If for any reason that the program access through ERFIS

was unable, the procedure indicated that a computer with the program

installed on its hard drive could be used.

In order to ensure that the operators were capable of accessing the

program, under worst case conditions, the inspectors requested the

Control Room operators to demonstrate use of the program assuming that

ERFIS was out-of-service. The operators indicated that the dose program

was installed on several of their non-ERFIS Control Room computers.

When the operators attempted to access the program via the backup method

in accordance with step 1.1.8 of the procedure. they were unsuccessful.

The Information Technology (IT)

Manager, who's organization provides

computer support, was contacted to discuss the problems encountered.

After a lengthy discussion, the operators were able to eventually access

the dose program from a different computer subdirectory than that

31

specified by EPRAD-03. The licensee indicated that the procedure would

be revised to correct the steps for backup access to the program.

Also, during the unsuccessful attempts to access the program, the Shift

Supervisor produced a computer disk that was stored in his desk that

contained the dose program. This disk was loaded into a Control Room

computer and the program was successfully run, however, the inspectors

noted that the program was not the correct revision. The Shift

Supervisor indicated that the disk had been in the desk for a

considerable time. The disk was later confirmed to be an uncontrolled

copy of the program and was subsequently removed from circulation and

destroyed. The licensee's search for other uncontrolled disks did not

result in any being found. A site wide memo was later distributed

reminding personnel that unauthorized or uncontrolled computer disks

should not be in circulation. The inspectors determined that adequate

corrective actions were taken or planned for this uncontrolled disk

issue.

The inspectors determined that the instructions contained in EPRAD-03

were inadequate for accessing the dose projection program using the

backup method from the Control Room. While the inspectors agreed that

it was highly unlikely that the ERFIS related access to the program

would be unavailable, it was a possibility. As such, the operators

needed to have a reliable backup method for accessing the program and

performing the necessary dose calculations in a timely manner (i.e..

prior to Emergency Response Team arrival). This issue was identified as

example three of Violation VIO 50-261/96-11-01:

Failure to Follow or

Inadequate Procedures - Three Examples.

c. Conclusions

The inspectors concluded that the licensee had established procedures

and controls for the capability to conduct on-shift dose assessments

during accident situations. A procedure discrepancy was identified with

the backup method for accessing the computer software for calculating

dose projections in the Control Room. This issue was identified as

example three of a violation for inadequate procedures.

V. Management Meetings

X1

Exit Meeting Summary

The inspectors presented the inspection results to members of licensee

management at the conclusion of the inspection on October 8. 1996. Interim

exits were conducted on August 23, 28, and September 20, 1996. The licensee

acknowledged the findings presented.

The inspectors asked the licensee whether any materials examined during the

inspection should be considered propriet'ary. No proprietary information was

identified.

32

PARTIAL LIST OF PERSONS CONTACTED

Licensee

J. Clements, Manager, Site Support Services

D. Crook. Senior Specialist, Licensing/Regulatory Compliance

C. Hinnant, Vice President, Robinson Nuclear Plant

J. Keenan, Director, Site Operations

R. Krich. Manager. Regulatory Affairs

B. Meyer, Manager. Operations

G. Miller, Manager, Robinson Engineering Support Services

R. Moore, Manager. Outage Management

J. Moyer. Manager. Maintenance

D. Stoddard. Manager, Operating Experience Assessment

R. Warden, Acting Manager, Nuclear Assessment Section

T. Wilkerson, Manager, Environmental Control

D. Young, General Manager, Robinson Plant

NRC

J. Zeiler, Acting Senior Resident Inspector

P. Byron. Resident Inspector, Surry

33

INSPECTION PROCEDURES USED

IP 37551:

Onsite Engineering

IP 62700:

Maintenance Implementation

IP 62707:

Maintenance Observation

IP 71707:

Plant Operations

IP 71750:

Plant Support Activities

IP 83750:

Occupational Radiation Exposure

IP 84750:

Radioactive Waste Treatment, and Effluent and Environmental

Monitoring

IP 86750:

Solid Radioactive Waste Management and Transportation of

Radioactive Materials

IP 92902:

Followup - Maintenance

IP 92903:

Followup - Engineering

IP 93802:

Prompt Onsite Response to Events at Operating Power Reactor

T12515/133: Implementation of Revised 49 CFR Parts 100-170 and 10 CFR Part

ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

Type

Item Number

Status

Description and Reference

VIO

50-261/96-11-01

Open

Failure to Follow or Inadequate Procedures

-Three

Examples (Sections 01.7. N1.l, and

P3.1)

VIO

50-261/96-11-02

Open

Inadequate Corrective Actions to Prevent

Expired Fire Brigade Medical Physicals

(Section 01.8)

NCV

50-261/96-11-03

Open

Failure to follow procedures for personnel

contamination monitoring (Section R1.2)

IFI

50-261/96-11-04

Open

Review Licensee RMS Sample Line

Particulate Deposition and Iodine Plate

out Evaluations: and R-14 Qualification to

Expected Accident Doses (Section R7.1)

Closed

e

Item Number

Status

Description and Reference

LER

50-261/94-16-01

Closed

Reactor Trip Due to Loss of Load (Section

08.1)

LER

50-261/93-16-00

Closed

Ventilation System Outside Design Basis

Due to Positive Pressure Condition

(Section M8.1)

34

Type

Item Number

Status

Description and Reference

(cont'd)

LER

d

21~26

3-

00 Closed

Technical Specification Violation Due to

Missed Channel Functional Test (Section

M8.2)

IFI

50-261/94-028O03 Closed

Follow Licensee's Activities to Enhance

The On-Line Maintenance Scheduling Process

(Section M8.3)

IFI

50-261/95-20-01

Closed

Justification of Time Required to

Establish Alternate SI Pump Thrust Bearing

Cooling (Section E8.1)

IFI

50-261/95-2002

Closed

Evaluation of Air Operated Valves "Smart

Failures" (Section E8.2)

NCV

50-261/96-11-03

Closed

Failure to follow procedures for personnel

contamination surveys (Section R1.2)