ML14178A355

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Insp Rept 50-261/93-10 on 930417-0514.Violations Noted. Major Areas Inspected:Operational Safety Verification, Surveillance Observation,Maint Observation,Loss of DHR & Followup
ML14178A355
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 06/08/1993
From: Christensen H, Garner L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14178A353 List:
References
50-261-93-10, NUDOCS 9307020169
Download: ML14178A355 (13)


See also: IR 05000261/1993010

Text

p5 V%

REG&y

UNITED STATES

0

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

Report No.:

50-261/93-10

Licensee:

Carolina Power and Light Company

P. 0. Box 1551

Raleigh, NC

27602

Docket No.:

50-261

License No.: DPR-23

Facility Name:

H. B. Robinson Unit 2

Inspection Conducted: April 17 - May 14, 1993

Lead Inspector:

41

7

9>

7127

L. W. Garner, Senior Resident Inspector

at Signed

Other Inspector:/. R Ogle, Resident Inspector

Approved ky: 471 -i

3

C ristensen, Chief

at Signed

Reacto Projects Section 1A

Division of Reactor Projects

SUMMARY

Scope:

This routine, unannounced inspection was conducted in the areas of operational

safety verification, surveillance observation, maintenance observation, loss

Results:

A violation was identified for failure to prescribe appropriate procedures

to verify the proper operation of the AMSAC A microprocessor after its

replacement (paragraph 5).

A non-cited violation was identified, in that, the provisions of Technical

Specification 6.2.3.b regarding authorization of-shift-work hours in excess of

those specified was not implemented (paragraph 6).

An inspector followup item was identified concerning spare part availability

for the Anticipated Transient Without Scram Mitigation Actuation Circuitry

System (paragraph 5).

9307020169 930608

PDR

ADOCK 05000261

Q

PDR

2

Greater than 10 gpm Reactor Coolant System leakage from a charging pump

relief valve resulted in a Notice Of Unusual Event emergency classification

(paragraph 6).

While inspecting the inside of a emergency diesel generator panel, the

inspectors observed that a capacitor in the voltage regulator circuit was

damaged (paragraph 3).

REPORT DETAILS

1.

Persons Contacted

  • D. Bauer, Regulatory Compliance Coordinator, Regulatory Compliance
  • B. Clark, Manager, Maintenance
  • T. Cleary, Manager, Technical Support
  • D. Crook, Senior Specialist, Regulatory Compliance

C. Dietz, Vice President, Robinson Nuclear Project

R. Downey, Shift Supervisor, Operations

J. Eaddy, Manager, Environmental and Radiation Support

S. Farmer, Manager - Engineering Programs, Technical Support

R. Femal, Shift Supervisor, Operations

  • W. Flanagan Jr., Acting Plant General Manager, Robinson Nuclear Project
  • W. Gainey, Manager, Plant Support
  • H. Habermeyer, Vice President, Nuclear Services
  • J. Harrison, Manager, Regulatory Compliance

D. Knight, Shift Supervisor, Operations

  • A. McCauley, Manager - Electrical Systems, Technical Support

R. Moore, Acting Manager - Shift Operations, Operations

D. Morrison, Shift Supervisor, Operations

  • P. Musser, Manager - Engineering/Technical Support, Nuclear Assessment

Unit

  • A. Padgett, Manager, Environmental and Radiation Control

E. Shoemaker, Manager, Mechanical Systems, Technical Support

W. Stover, Shift Supervisor, Operations

  • D. Taylor, Manager, Materials &-Contract Services
  • A. Wallace, Acting Manager, Operations
  • L. Williams, Manager, Security

D. Winters, Shift Supervisor, Operations

Other licensee employees contacted included technicians, operators,

engineers, mechanics, security force members, and office personnel.

  • Attended exit interview on May 24, 1993.

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2. Plant Status

Except for a power reduction to perform turbine generator valve testing,

the unit operated at full power during the report period. RCS leakage

greater-than 10 gpm from the A charging pump stabilizer relief valve

resulted in the unit being in a NOUE emergency classification for

approximately four and one-half hours on May 12, 1993. See paragraph 3

for additional information.

2

3. Operational Safety Verification (71707)

The inspectors evaluated licensee activities to confirm that the

facility was being operated safely and in conformance with regulatory

requirements. These activities were confirmed by direct observation,

facility tours, interviews and discussions with licensee personnel and

management, verification of safety system status, and review of facility

records.

To verify equipment operability and compliance with TS, the inspectors

reviewed shift logs, Operation's records, data sheets, instrument

traces, and records of equipment malfunctions. Through work

observations and discussions with Operations staff members, the

inspectors verified the staff was knowledgeable of plant conditions,

responded properly to alarms, adhered to procedures and applicable

administrative controls, cognizant of in-progress surveillance and

maintenance activities, and aware of inoperable equipment status. The

inspectors performed channel verifications and reviewed component status

and safety-related parameters to verify conformance with TS. Shift

changes were routinely observed, verifying that system status continuity

was maintained and that proper control room staffing existed. Access to

the control room was controlled and operations personnel carried out

their assigned duties in an effective manner. Control room demeanor and

communications were appropriate.

Plant tours and perimeter walkdowns were conducted to verify equipment

operability, assess the general condition of plant equipment, and to

verify that radiological controls, fire protection controls, physical

protection controls, and equipment tagging procedures were properly

implemented.

Security Force Member Vacated Compensatory Post

The inspectors reviewed the licensee's investigation report concerning

an alarmed door to a vital area that was left unattended with the alarm

function non-operational.

The incident occurred on April 22, 1993.

This incident will be followup by a regional security inspector.

Radiation Monitor Deficiencies

IR 93-08 discussed a 10 CFR Part 21 Report concerning a deficiency in

the electrical design of the process and area radiation monitors

utilized at the site. Specifically, an internal 5 volt power supply

could fail -without -the--failure-being annunciated. -However, the loss of

this power supply would also result in the loss of the digital readout

and thus was readily detectable. The vendor, Nuclear Research

Corporation, designed a circuit change to correct the deficiency. The

change involved installation of a jumper on the printed circuit boards

associated with the ratemeters. By April 21, all 22 radiation monitors

had been modified. The inspectors witnessed portions of the tests

performed to return the radiation monitors to service. The modified

units appeared to function correctly.

3

A EDG Partial Start During Barring Evolution

IR 93-07 described an events in which during barring over of the A EDG,

the engine speed began to rapidly increase and the engine was shutdown

by the operator. The barring evolution after each EDG run was a vendor

recommendation. The barring clears lube oil from the top of the bottom

pistons, i.e., reduces the likelihood of an exhaust manifold fire during

a subsequent start.

During this report period, additional testing was performed to recreate

the events and determine probable cause. The licensee utilized a

Woodward governor vendor representative to assist in this effort. The

testing verified that the governor will move the fuel racks partially

open and then if the operator does not intervene, the fuel racks will

subsequently close. Thus, operator action was not required to shut the

engine down before it reached full speed. The inspectors witnessed

performance of some of the tests and reviewed the operation of the

governor with the vendor representative. From a schematic which shows

the hydraulic operation of the governor, the observed phenomena was not

explainable. No diagram was available which showed the actual flow

paths and design of the internal components and clearances. The vendor

representative indicated that the phenomena was not unheard of and that

adjustment to shutdown solenoid may correct this condition. Both the

vendor representative and the cognizant engineer continued to support

the licensee's position that thle phenomena did not adversely affect the

function of the governor, i.e., the A EDG. The inspectors agreed with

their assessment. Engineering was evaluating replacing the governor

with one from stock and shipping the governor to the vendor for bench

testing. The inspectors will continue to monitor the licensee's efforts

in this area.

Failure Of Capacitor C-8 in A EDG Voltage Regulator Circuit

On April 26, 1993, the inspectors observed that capacitor C8 on the EDG

A voltage regulator circuit board was damaged. At the time of this

observation, the EDG was inoperable as a result of ongoing maintenance

and testing. A subsequent inspection by the licensee confirmed the

inspectors observation and the capacitor was replaced later that day.

To ensure no collateral damage to other components in the voltage

regulator circuit, the licensee also performed a satisfactory resistance

check of diode CR8 in the voltage regulator circuit on April 28, 1993.

The EDG was returned to service on April 29, 1993, following

satisfactory operation of the voltage regulator at an EDG loading of

2500 KW during performance of OST-401.

Capacitor C8 was wired across a rectifier bridge in the automatic

voltage regulator circuit for the EDG. After analyzing the regulator

circuit and discussions with the voltage regulator vendor, the licensee

stated that the damaged capacitor acted as a filter for the output of

the rectifier bridge. The licensee also stated their conclusion that

failure of the capacitor would not adversely impact the ability of the

regulator circuit to perform its function. Additionally, the licensee

4

concluded that if collateral damage occurred to the circuit with the

failure of C8, the most likely component to be degraded would be diode

CR8.

The inspectors independently reviewed the circuit schematic and, after

discussions with NRC Region II staff, concurred with the licensee's

conclusion regarding the function of the capacitor. The inspectors also

concurred with the licensees conclusions regarding diode CR8 as the most

likely component for collateral damage. The inspectors witnessed the

replacement of the capacitor per WR/JO-AEWW1 and the restoration of EDG

A to service in accordance with OST-401. The inspectors also reviewed

the results of the satisfactory electrical checks on diode CR8. The

inspectors have no further question on this issue at this time.

B Fuel Oil Transfer Pump Frequent Cycling

At 9:36 p.m. on April 27, 1993, during an operability run of B EDG in

accordance with OST-409, operators noted that B fuel oil transfer pump

was cycling frequently. The pump was observed to run for 30 seconds out

of every two minutes. At the time of this observation, A EDG was

inoperable as a result of ongoing repair/testing activities associated

with failed capacitor C8 and the barring anomaly discussed in the

preceding paragraphs. An operability determination was initiated for

the B fuel transfer pump at 10:43 p.m. on April 27, 1993.

At 4:59 p.m.

on April 29, 1993, following the restoration of EDG A to service, B EDG

was declared inoperable and TS 3.7.2.d LCO was entered to allow repairs

to the day tank level circuitry. The LCO allowed operation to continue

for seven days before placing the reactor in hot shutdown. Following

replacement of the day tank low level switch, B EDG was returned to

service at 10:30 p.m. on April 29, 1993, and the TS LCO was exited. The

operability determination was completed at 10:18 p.m. on April 29, 1993,

and concluded that the fuel oil transfer pump and its associated

starting circuitry components would continue to operate satisfactorily

at the observed cycling frequency.

The inspectors independently reviewed the operability determination and

the completed work request and have no further question at this time.

No violations or deviations were identified.

4. Surveillance Observation (61726)

The inspectors observed certain safety-related surveillance activities

on systems-and components to ascertain that-these activities were

conducted in accordance with license requirements. For the surveillance

test procedures listed below, the inspectors determined that precautions

and LCOs were adhered to, the required administrative approvals and

tagouts were obtained prior to test initiation, testing was accomplished

by qualified personnel in accordance with an approved test procedure,

test instrumentation was properly calibrated, the tests were completed

at the required frequency, and that the tests conformed to TS

requirements. Upon test completion, the inspectors verified the

5

recorded test data was complete-, accurate, and met TS requirements, test

discrepancies were properly documented and rectified, and that the

systems were properly returned to service. Specifically, the inspectors

witnessed/reviewed portions of the following test activities:

OP-604

Operating Procedure Diesel Generators A and B

(Section 8.6: Barring Over Diesel Generator A)

OST-051

Reactor Coolant System Leakage Evaluation

OST-352

Containment Spray System Component Test

OST-409

Emergency Diesels (Rapid Speed Start)

OST-401

Emergency Diesels (Slow Speed Start)

No violations or deviations were identified. Based on the information

obtained during the inspection, the area/program was adequately

implemented.

5. Maintenance Observation (62703)

The inspectors observed safety-related maintenance activities on systems

and components to ascertain that these activities were conducted in

accordance with TS and approved procedures. The inspectors determined

that these activities did not violate LCOs and that required redundant

components were operable. The inspectors verified that required

administrative, material, testing, radiological, and fire prevention

controls were adhered to. In particular, the inspectors

observed/reviewed the following maintenance activities:

WR/JO 93-AEWW1

Replace Capacitor C-8 On A EDG

Voltage Regulator Circuit Card

WR/JO 93-ADFN1

Replace Mechanical Seal On A EDG

Standby Coolant Pump

WR/JO 93-AEMQ1

Troubleshoot A EDG Control Circuit

Inadequate Post-Maintenance Testing Of AMSAC

IR 93-07 discussed the March 31, 1993, failure of both AMSAC channels.

Due to the unavailability of spare parts, only the A channel was

repaired-and returned to service on April 10.--The repair was

accomplished by replacement of the A channel microprocessor.

Satisfactorily performance of the new microprocessor was considered to

be demonstrated by performance of SP-1198, AMSAC System Test (At Power).

On April 20, the inspectors reviewed SP-1198 and determined that it did

not functionally test the entire A channel.

During subsequent

discussions with engineering personnel, the inspectors were informed

that the circuitry not tested by SP-1198 was periodically, automatically

tested by AMSAC's self-test feature. The inspectors requested the

6

licensee provide documentation which would described the self-test

feature in sufficient detail such that one could verify that the entire

circuitry had been tested. While reviewing the applicable sections of

the AMSAC vendor manual, the licensee discovered that the self-test

feature of a channel was not performed when the other channel's

microprocessor is out of service. Since the B channel microprocessor

was not functional, portions of the A channel remained untested after it

was returned to service on April 10.

Essential elements of the A

channel that were not tested included the logic output contacts.

SP

1198 was revised to perform a complete logic test of the A channel.

Satisfactorily performance of the revised SP-1198 was witnessed by the

inspectors on April 23.

Operability and testing of AMSAC was not addressed in TS. However, the

system was required to be installed by 10 CFR 50.62 and thus is

considered as important to safety. Failure to provide an adequate test

procedure for testing essential elements of the circuitry associated

with the replaced microprocessor constituted a failure to establish

procedures appropriate to the circumstances as required by 10 CFR 50

Appendix B Criterion V. This is identified as a VIO: Failure To

Establish Adequate Procedures To Verify Proper AMSAC Operation After

Microprocessor Replacement, 93-10-01.

As discussed above, the B channel was not returned to service at the

time the A channel was placed in service due to the unavailability of

another microprocessor. A microprocessor was obtained from the vendor,

Modicon Sealed Support Center, and the B channel was successfully tested

and returned to service on May 7. However, the vendor has no additional

microprocessors in stock and no longer manufactures this component.

Apparently, the AMSAC system installed at the site was installed in only

two other nuclear facilities. HBR was unable to obtain from either of

these two sites a spare microprocessor that was compatible with the

system installed here. Hence, for future failures availability of parts

to repair AMSAC in a timely manner was a concern. At the end of the

report period, the licensee had initiated efforts to address this

concern. This item is identified as an IFI: Lack Of Spare Parts Could

Result In Prolonged Unavailability Of AMSAC, 93-10-02.

One violations was identified. Except as noted above, the area/program

was adequately implemented.

6. Event Followup (92701, 93702)

At 6:13 p.m.-on May-12,.-1993, an NOUE was declared,. in accordance with

EAL-2 flowchart criteria, for RCS leakage greater than 10 gpm. At 8:54

p.m. A charging pump and associated piping was isolated after it was

determined to be the source of the leakage. Utilizing OST-051, the RCS

leakage rate was confirmed to less than 10 gpm, i.e., had decreased to

0.0796 gpm. The NOUE was exited at 10:36 p.m..

The inspectors were notified of the event via the licensee's beeper

notification system. The inspectors reported to the site and from

7

approximately 6:45 p.m. to 11:00 p.m. witnessed the licensee's event

response. The inspection included observations both in the control

room, the OSC, and the TSC. In general, the response was deemed

satisfactory. The inspectors also verified that state, local, and NRC

notifications were performed in accordance with regulatory requirements.

The source of the leakage was determined to be the A charging pump

suction relief valve, CVC-2080. An inspection of the valve by the

licensee revealed that the setpoint adjusting bolt nut had loosened from

its snug position against the bonnet face. This allowed the adjusting

bolt to loosen and resulted in a lowering of the valve lift setpoint

from 75 psig to 10 psig. The valve was disassembled and inspected;

however, the cause of the loose adjusting bolt nut could not be

definitely determined. The root cause of the loose adjusting nut will

be addressed by the licensee as part of the ACR process. During the

inspection light scoring was observed on the valve disc. Following

replacement of the disc, nozzle, and spindle, the valve was

satisfactorily retested and reinstalled in the system.

An inspection of the suction relief valves for the B and C charging

pumps indicated that the adjusting bolt nuts for those valves were in

the correct position. A review of plant and industry experience by the

licensee, as well as, discussions with the valve vendor failed to reveal

any prior occurrences of this problem. Thus, the licensee considered

this an isolated event.

The inspectors witnessed a portion of the repair and testing efforts

associated with the A charging pump suction relief valve. Additionally,

the inspectors reviewed WR/JO 92-AKWG1, under which the last maintenance

was performed on CVC-2080 on October 9, 1992.

No abnormalities were

identified in that WR/JO which could have resulted in the loose

adjusting nut.

On May 13, a licensee review identified that during the event, key

personnel had exceeded the working hour guidelines of TS 6.2.3.b.

without approval from the Plant General Manager or his designee.

Specifically, the TS guideline states that "An individual should not be

permitted to work more than ...

24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> in any 48-hour period ...

excluding shift turnover time. Any deviation from the above guidelines

shall be authorized by the Plant General Manager or his designee ...

in

accordance with established procedures..." PLP-015, Program For Nuclear

Power Plant Staff Working Hours, implements this requirement. ACR 93

084 was initiated to address this TS violation. This violation will not

be subject to enforcement- action because the-licensee's efforts in

identifying and correcting the violation meet the criteria specified in

Section VII.B of the Enforcement Policy. Thus, this item is identified

as a NCV: Failure To Authorize Shift Work Hours In Excess Of Those

Specified In TS 6.2.3.b, 93-10-03.

One NCV was identified. Except as noted above, the area/program was

adequately implemented.

8

7. Loss Of Decay Heat Removal (TI 2515/103)

By letter dated February 1, 1989, the licensee described commitments to

address the six programmed enhancement recommendations identified in GL 88-17. The inspectors verified that M-1011, Instrumentation For Midloop

Operation, installed instrumentation for midloop operation as committed

in their February 1, 1989 letter. The inspectors also verified that

requirements for equipment availability and key parameter monitoring

were contained in GP-008, Draining The Reactor Coolant System, and OMM

030, Control Of CV Penetrations During Midloop Operation as required.

Current procedures did not allow perturbations of the RCS and thus

additional procedures were not necessary to address this area. The

inspectors also reviewed the February 1, 1989 response against the six

items discussed in GL 88-17. Based upon the inspection activities, the

inspectors concluded that licensee met the intent of GL 88-17 items 1

through 4 and 6 by a combination of procedure revisions and new hardware

installations. In response to item 5, the licensee determined that no

TS changes were required. This temporary instruction is considered

closed.

8. Followup (92701, 92702)

(Closed) VIO 92-11-01, Failure To Implement FP-005 Resulted In Alert

Declaration. The inspectors confirmed that FP-005, Hot Work Permit, was

revised to help ensure that all actions required to be performed prior

to work authorization are completed. Training records were reviewed to

confirm that designated plant personnel were trained on the procedure

revision. In addition, the inspectors verified that ACRs92-284, 285

and 291 were initiated to review other key plant work processes, i.e.,

RWPs, confined space and equipment clearance programs. The reviews

required by these ACRs have been completed. The inspectors noted that

action items were identified to address the ACR findings; however, the

inspectors did not review the adequacy of the proposed corrective

actions for the these findings. This item is considered closed.

(Closed) VIO 92-11-03, Failure To Implement Appropriate Instructions

During SW 374 and 376 Valve Maintenance. The inspectors verified that

the current revisions of MMM-001, Maintenance Administration Program,

and MMM-003, Maintenance Work Requests, contained the information

specified in the Reply To A Notice Of Violation, dated July 1, 1992.

Specifically, MMM-001 step 5.5.14 required Technical Support perform a

seismic review prior to removal of a safety related component that

results in loose piping or anchorage. MMM-003 Attachment 6.5, Work

Request-Planning-Checklist, referenced MMM-001-step 5.5.14 if a safety

related component is to be removed. These actions should preclude

recurrence of this violation. This item is considered closed.

(Closed) VIO 92-11-05, Failure To Translate RHR System Design Basis Into

M-1087. The inspectors verified that the following corrective actions

were adequately implemented as committed in the Reply To A Notice Of

Violation, dated July 1, 1992. RHR System DBD and SD-003, Residual Heat

Removal, were revised. A memorandum was issued to engineering personnel

9

requiring that when a modification is released to the plant for review,

a marked up copy of each affected plant procedure accompany the

transmittal.

NED procedure 3.3, Design Verification/Technical Review,

was established to institute a formal qualification program for

engineering personnel. This item is considered closed.

(Closed) VIO 92-16-03, CM-508 Was Not Adequately Established In That

Steps Provided For EDG Fuel Filter Assembly Were Out Of Sequence And

Failure To Adequately Establish Procedure CM-303 For EQ Splices. The

inspectors verified that CM-303 and CM-508 were revised as necessary to

provide adequate instructions for their respective activity. MI-506-0,

Maintenance Procedures Program, was implemented, as committed in the

Reply To A Notice Of Violation, dated August 20, 1992, to require

validation of procedure revisions. In addition, MI-506-0 addressed

tracking and trending of the validation process to determine the

effectiveness of the program. This item is consider closed.

(Closed) VIO 92-16-04, Instructions In M-1128 Were Not Appropriate To

The Circumstances In That The Modification Created An Unmonitored

Release Pathway. The inspectors reviewed the Reply To A Notice Of

Violation dated August 20, 1992. The inspectors verified that the

procedure were revised or in the process of being revised as committed

in the reply. Specifically, the inspectors verified that Attachment

6.3, Review Assignment Criteria, of AP-22, Document Change Procedure,

revision 11, dated March 27, 1993, required evaluation for unmonitored

release pathways. The inspectors also verified that a check sheet had

been issued for interim use until a similar change could be implemented

into the Nuclear Plant Modification Program manual.

These actions

should be sufficient to preclude recurrence of this event. This item is

considered closed.

No violations or deviations were identified. Based on the information

obtained during the inspection, the area/program was adequately

implemented.

9. Exit Interview (71701)

The inspection scope and findings were summarized on May 24, 1993, with

those persons indicated in paragraph 1. The inspectors described the

areas inspected and discussed in detail the inspection findings listed

below and in the summary. Dissenting comments were not received from

the licensee. The licensee did not identify as proprietary any of the

materials provided to or reviewed by the inspectors during this

inspection.

Item Number

Description/Reference Paragraph

93-10-01

VIO - Failure To Establish Adequate Procedures

To Verify Proper AMSAC Operation After

Microprocessor Replacement (paragraph 5).

10

93-10-02

IFI - Lack Of Spare Parts Could Result In

Prolonged Unavailability Of AMSAC (paragraph 5).

The following NCV was identified and reviewed during this inspection

period.

Item Number

Description/Reference Paragraph

93-10-03

Failure To Authorize Shift Work Hours In Excess

Of Those Specified In TS 6.2.3.b (paragraph 6).

10.

List of Acronyms and Initialisms

a.m.

Ante Meridiem

ACR

Adverse Condition Report

AMSAC

ATWS Mitigation System Actuation Circuitry

AP

Administrative Procedure

CFR

Code of Federal Regulations

CM

Corrective Maintenance

CV

Containment Vessel

CVC

Chemical & Volume Control

DBD

Design Basis Documentation

EAL

Emergency Action Level

EDG

Emergency Diesel Generator

EQ

Environmental Qualification

FP

Fire Protection

gpm

Gallons Per Minute

GL

Generic Letter

GP

General Procedure

HBR

H. B. Robinson

IFI

Inspector Followup Item

IR

Inspection Report

KW

Kilowatt

LCO

Limiting Condition for Operation

M

Modification

MI

Maintenance Instruction

MMM

Maintenance Management Manual

NCV

Non-cited Violation

NED

Nuclear Engineering Department

NOUE

Notice of Unusual Event

NRC

Nuclear Regulatory Commission

OMM

Operations Management Manual

OP

Operations Procedure

OSC

Operations Support Center

OST

Operations Surveillance Test

p.m.

Post Meridiem

PLP

Plant Program

Psig

Pounds per square inch - gage

RCS

Reactor Coolant System

RHR

Residual Heat Removal

RWP

Radiation Work Permit

SD

System Description

11

SP

Special Procedure

SW

Service Water

TI

Temporary Instruction

TS

Technical Specification

TSC

Technical Support Center

VIO

Violation

WR/JO

Work Request/Job Order