ML14178A088

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Insp Rept 50-261/91-01 on 910111-0215.Violations Noted.Major Areas Inspected:Operational Safety Verification,Installation & Testing of Mods,Surveillance & Maint Observations,Onsite Review Committee & Followup
ML14178A088
Person / Time
Site: Robinson Duke Energy icon.png
Issue date: 03/05/1991
From: Christensen H, Garner L
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION II)
To:
Shared Package
ML14178A086 List:
References
50-261-91-01, 50-261-91-1, NUDOCS 9103250215
Download: ML14178A088 (28)


See also: IR 05000261/1991001

Text

1 pkREGU4

UNITED STATES

o

NUCLEAR REGULATORY COMMISSION

REGION II

101 MARIETTA STREET, N.W.

ATLANTA, GEORGIA 30323

ReMp

No.: 50-261/91-01

Licensee:

Carolina Power and Light Company

P. 0. Box 1551

Raleigh, NC 27602

Docket No.:

50-261

License No.: DPR-23

Facility Name: H. B. Robinson

Inspection Conducted: January 11 -

February 15, 1991

Lead Inspector: 2"o -/

L. W. Garne 1, Senior Resident I pector

Date Sygned

Other Inspectors: R. E. Carroll

M. M. Glasman

K. R Jury

Approved by:

da 0iUrust3

1

,H.

0. [Christensen, Chief

D e Gigned

Reactor Projects Branch 1

Division of Reactor Projects

SUMMARY

Scope:

This routine, announced inspection was conducted in the areas of operational

safety verification, installation and testing of modifications, surveillance

observation, maintenance observation, onsite review committee, and followup.

Results:

A violation with two examples was identified for failure to accomplish

activities affecting quality in accordance with procedures or drawings.

The

first example involved maintenance technicians' failure to perform modification

acceptance testing as documented, which resulted in the improper declaration of

modification operability (paragraph

3).

The second example involved an

incorrect size fuse being installed in the A SI pump control circuit other than

that shown on the applicable drawing (paragraph 5).

A violation was identified for inadequate modification acceptance tests being

specified for component functional verification (paragraph 3).

9103250215 910305

PDR

ADOCK 05000261

PDR

2

A violation was identified involving an inadequate procedure change to test

the main steam line isolation function.

This indicated a weakness in the

preparation and technical review process associated with logic testing

procedures (paragraph 4).

A non-cited violation was identified for failure of a worker to be dressed in

accordance with radiation work permit requirements (paragraph 2).

ASME Code relief was granted to operate cycle 14 with engineered repairs to

service water containment penetrations

and

piping inside containment

(paragraph 2).

Preliminary closeout inspections of the containment indicated that the cleanup

was not being performed in a thorough, systematic manner (paragraph 2).

Two service water system spills in containment and the auxiliary building

were apparently caused by unanticipated valve seat movement (paragraph 2).

The recovery evolution for an unlatched control rod was well planned and

executed (paragraph 2).

Two drawing discrepancies were identified.

A reactor protection system

drawing incorrectly identified the source of power to the reactor trip breaker

circuit.

A safeguards logic diagram did not indicate that an automatic

containment spray initiation signal would also initiate a safety injection

signal (paragraph 2).

A green liquescent substance originating from Machine Tool wiring was

discovered on contactors inside class 1E motor control centers.

This was

identified as the probable cause of two valves failing to operate properly

(paragraph 5).

The licensee is developing a fuse schedule as part of the development of an

overall fuse control program (paragraph 5).

A commitment was not met to develop a Plant Specific Technical Guideline by

September 28, 1990, in that the basis for some setpoints were not established

(paragraph 7).

REPORT DETAILS

Persons Contacted

  • R. Barnett, Manager, Outages and Modifications

C. Baucom, Shift Outage Manager, Outages and Modifications

  • D. Bauer, Regulatory Compliance Coordinator, Regulatory Compliance

J. Benjamin, Shift Outage Manager, Outages and Modifications

C. Bethea, Manager, Training

  • W. Biggs, Manager, Nuclear Engineering Department Site Unit
  • S. Billings, Technical Aide, Regulatory Compliance
  • R. Chambers, Manager, Operations

T. Cleary, Manager - Balance of Plant Systems and Reactor Engineering,

Technical Support

  • D. Crook, Senior Specialist, Regulatory Compliance
  • J.

Curley, Manager, Environmental and Radiation Control

  • C. Dietz, Manager, Robinson Nuclear Project
  • D. Dixon, Manager, Control and Administration

J. Eaddy, Manager, Environmental and Radiation Support

F. Eckert, Manager, Planning and Scheduling, Outages and Modifications

S. Farmer, Manager - Engineering Programs, Technical Support

R. Femal, Shift Supervisor, Operations

B. Harward, Manager - Mechanical Systems, Technical Support

  • J.

Kloosterman, Manager, Regulatory Compliance

D. Knight, Shift Supervisor, Operations

  • D. Labelle, Project Engineer, Nuclear Assessment

E. Lee, Shift Outage Manager, Outages and Modifications

  • A. McCauley, Manager - Electrical Systems, Technical Support

R. Moore, Shift Supervisor, Operations

D. Nelson, Shift Outage Manager, Outages and Modifications

  • M. Page, Manager, Technical Support

D. Seagle, Shift Supervisor, Operations

  • J. Sheppard, Plant General Manager
  • R. Smith, Manager, Maintenance
  • D. Stadler, Onsite Licensing Engineer, Nuclear Licensing

R. Steele, Shift Supervisor, Operations

  • D. Stepps, Senior Engineer, Nuclear Engineering Department Site Unit
  • G. Walters, Operating Event Followup Coordinator, Regulatory Compliance

D. Winters, Shift Supervisor, Operations

H. Young, Manager, Quality Control

Other licensee employees contacted included technicians, operators,

mechanics, security force members, and office personnel.

  • Attended exit interview on February 25, 1991.

2

H. Christensen, Section Chief, Division of Reactor Projects, Region II

was on site January 22-24, 1991, to meet with the resident inspectors and

plant management.

Acronyms and initialisms used throughout this report are listed in the

last paragraph.

2. Operational Safety Verification (71707)

The inspectors evaluated licensee activities to confirm that the facility

was being operated safely and in conformance with regulatory

requirements.

These activities were confirmed by direct observation,

facility tours, interviews and discussions with licensee personnel and

management, verification of safety system status, and review of facility

records.

To verify equipment operability and compliance with TS,

the inspectors

reviewed Operations' records, data sheets, instrument traces, and records

of equipment malfunctions.

Through work observations and discussions

with Operations Staff members,

the inspectors verified the staff was

knowledgeable of plant conditions, cognizant of in-progress surveillance

and maintenance activities, and aware of inoperable equipment status.

The inspectors reviewed component status and safety-related parameters to

verify conformance with TS.

The inspectors observed that proper control

room staffing existed, access to the control room was controlled, and

Operations personnel carried out their assigned duties in an effective

manner.

Plant tours and perimeter walkdowns were conducted to verify equipment

operability, assess the general condition of plant equipment,

and to

verify that radiological controls, fire protection controls, physical

protection controls,

and equipment tagging procedures were properly

implemented.

Unlatched Control Rod

On January 29,

1991,

during performance of EST-048,

Control Rod Drop

Test,

RCCA C-07 exhibited an abnormal rod drop trace and time.

The

initial belief was that some equipment malfunction, such as a loose

monitoring lead connection, had caused the abnormal indications.

Repeat

testing on the next day produced similar results (i.e., the trace was not

a smooth curve and the rod took approximately one second longer to fall

than anticipated).

On January 31, 1991, the inspectors witnessed SP-1012,

Control Rod Drive Mechanism C-07 Testing, which verified that the C-07

drive shaft was uncoupled from its RCCA.

This was based upon the rod

lift,

moveable gripper and stationary gripper coil current traces, as

well as sound traces which demonstrated that the C-07 drive shaft

reached its maximum and minimum position three steps before three other

3

rods reached their respective maximum and minimum positions.

The C-07

lift

coil current also revealed that the lift

coil consistently moved its

drive shaft one step quicker (by approximately 20 milliseconds) than

other lift

coils raised their drive shafts one step (i.e., the C-07 lift

coil only had to move the weight of a drive shaft, not a drive shaft and

an RCCA).

Recovery of the unlatched control rod involved removal of the reactor

vessel head, as found inspection of C-07,

and video camera inspection of

the associated guide tube and RCCA. The inspectors witnessed performance

of SP-1016, Testing And Latching; Inspection And Unlatching Of The RCCA At

Core Location C-07, which confirmed by weighing that the C-07 drive shaft

was not attached to its associated RCCA. Subsequent testing revealed that

the drive shaft could be latched to the RCCA. A visual inspection of the

drive shaft revealed minor scratches and denting at the latching end of

the drive shaft.

Video camera inspection of the RCCA hub revealed only

superficial damage. There was not a condition found which could explain

the failure of the drive shaft to be latched to the RCCA. Video camera

inspection of the guide tube identified that it had been struck at several

locations by the drive shaft during rod drop testing.

The top of one

opening where the RCCA rodlets moves through the guide tube was determined

to be bent inwards.

Based upon the observed damage,

Westinghouse

recommended that the guide tube be replaced.

A new drive shaft and guide

tube were installed. The RCCA was inspected by video camera and partially

lifted to verify freedom of movement.

Based upon these results, the

RCCA was determined to be acceptable for continued service.

Prior to reactor vessel head installation, special verifications were

performed of each control rod to ensure by visual inspection and "go,

no-go" gaging that the drive shafts were set inside the RCCA hubs and the

latching buttons were properly engaged.

The inspectors noted that the

recovery evolution was well planned and executed.

Inadverent Removal of Source Assembly

On February 10,

1991, while moving the upper internals package for C-07

recovery evolutions,

the lift

was terminated when the control room

operator observed that source range monitor NI-31 count rate rapidly

decreased from 100 cpm to 20 cpm.

Visual inspection revealed four

rodlets hanging from under the upper internals package.

These rodlets

were determined to be an antimony-beryllium secondary source assembly.

At the time of discovery, the bottom of the upper internals package was

approximately 2 to 3 feet above the reactor vessel flange. The inspectors

witnessed successful performance of SP-1015,

Secondary Source Inspection

And Recovery.

The

SP provided instructions for lifting the upper

internals package sufficiently high enough to allow movement across the

reactor flange area with the 14 foot long source assembly attached and

subsequent removal of the source.

Movement across and positioning the

4

source above the refueling cavity floor was monitored by underwater

cameras.

Once positioned a few inches above the floor, a long rod was

used to reach inside the guide tube and lightly tap the top of the source

assembly.

The source assembly, weighing approximately 27 pounds, fell

uneventfully onto the cavity floor. The source assembly was subsequently

removed to the SFP for disposal.

The inspectors verified that ALARA and

radiation protection considerations were appropriately considered during

this evolution.

Root cause investigation attributed this event to an inadequate technical

review.

The source assembly was installed this RO in a different core

location,

H2,

than that previously utilized.

This particular location

does not have a flow vane installed in the top core plate as previous

locations did.

The flow vane presses down onto the source assembly,

thereby, keeping the assembly in place.

Without a flow vane installed,

the core differential pressure was sufficient to allow the light weight

source assembly to float up and wedge approximately eight inches inside

the upper internals package.

Corrective actions to preclude future

occurrences of positioning core components into undesirable locations are

under development.

As a result of not being able to reload this source into the core, there

is no irradiated source assembly installed in the core.

However, the

NI-31 and NI-32 count rates, approximately 20 cpm due to the presence of

irradiated fuel, are sufficient to allow a safe restart.

ASME Code Relief Request -

SW Piping

On January 6, 1991,

MIC was identified in the six inch diameter, schedule

40, 316L stainless steel weld joints in the SW supply and return piping of

containment fan cooler HVH-4. MIC indications were subsequently observed

in 11 of 16 HVH-4 piping weld joints radiographically examined.

The

affected HVH-4 piping contained a total of 53 weld joints.

One weld

joint was removed and taken to the HE & EC for analysis; the HE & EC

confirmed the presence of wall thinning due to MIC.

The MIC initiation

location was along the base metal/weld metal interface and the weld.

This location was different from the MIC previously observed in the 304L

stainless steel HVH SW return and supply piping, in that, the 304L MIC

had initiated in the weld joint heat affected zone adjacent to the weld.

During

RO 12, all the stainless steel HVH SW supply and return lines

inside the CV were replaced with AL6XN material except for the 316L piping

discussed above and inside the containment penetrations.

The HVH-4 SW

piping traversing under the refueling canal had been replaced in 1985 with

316L material.

All five 316L HVH-4 weld joints radiographically examined

in 1988 showed no MIC indications.

Radiographic examinations of the eight containment penetrations (a supply

and return penetration for each of the 4 containment fan coolers)

identified 4 penetrations with MIC.

The eight containment penetrations

5

had a 316L stainless steel liner installed in 1985 inside the 304L penetra

tion piping. The 304L penetration piping was fillet welded to the liner

and the 304L SW piping to the HVH units was then inserted over a portion

of the liner and fillet welded to the liner. During RO 12, the liners

were cut, the 304L piping from the CV side of the penetrations to the

HVH units was removed and replaced with AL6XN material.

The AL6XN piping

was inserted over the liner and fillet welded to it. This resulted in the

stainless steel liner being in contact with SW and having heat affected

zones acting as a containment boundary.

On January 16, 1991, the licensee requested an ASME code relief to allow

operation with temporary,

non-code,

engineered repairs to the above

described piping due to material availability and the long lead time

required for penetration repair technique development.

The engineered

repair consists of welded sleeves over all the 316L HVH-4 weld joints

which were not code repaired and welded sleeves over the piping of 4

containment penetrations which contained MIC indications.

The relief

request demonstrated that the unit could operate safely with the non-code

repairs.

The licensee committed (in the request) to replace the non-code

repaired 316L HVH-4 piping during RO 14 and submit to the NRC, a plan and

schedule for permanent repair of the containment penetrations by

September 30, 1991.

After review, the NRC granted the relief request on

January 23,

1991.

When the outage was extended as a result of an

unlatched control rod,

the inspectors verified that delivery dates

associated with the AL6XN elbows made it impractical to make permanent

code repairs to the HVH-4 during this RO.

SW Spills Into Containment and Auxiliary Building

On January 8, 1991, at 9:00 p.m.,

"significant leakage" was identified

coming from an open section of HVH-4 piping, and started flooding the first

level of the CV.

This open piping was caused by the removal of a section

of piping for MIC analysis. As operations was attempting to determine the

source of the water, the leak stopped with no apparent actions having been

initiated to terminate it

(i.e., valve manipulation/source isolation).

Upon evaluation, it was determined that approximately 12,000 gallons had

discharged into the CV sump. The SW system and the HVH-4 unit had been

isolated with proper clearances and drained prior to the piping removal.

An investigation and ACR 91-014 were initiated the next day to determine

the source and/or cause of the leak.

The system had no unisolated

potential leakage paths available that could have accounted for this

volume of water. A subsequent SW leak (see below) revealed the probable

flow path for this spill.

On January 17,

1991, during a SW system line-up for a hydrostatic test,

approximately 1600 gallons of SW leaked into the CV and Auxiliary Building

hallway. This leak occurred when the flange joint downstream of butterfly

6

valve V6-33E was separated, allowing the valve seat to shift out of the

valve. This allowed water to flow by the disc and pressurize the piping

downstream.

When the downstream piping associated with butterfly valve

V6-33D was subsequently opened, a leak path was created, allowing the

water to flow onto the Auxiliary Building floor. Additionally, there was

apparently a vent and drain valve open in the CV in preparation for the

hydrostatic test; thus allowing leakage into the CV.

Operations

subsequently isolated the leak and initiated ACR 91-040 to determine root

cause.

The seat movement associated with valve V6-33E evidently was the root

cause of both the January 8 and 17, spills.

In the January 8 spill, the

V6-33E flange joint was partially opened at a time which corresponds to

spill initiation. The licensee believes that the seat moved during this

event allowing water to flow around the disc and out the open section of

piping.

All the other HVH unit supply SW valves, as well as other SW

system valves, are Allis Chalmers Streamseal resilient seated butterfly

valves.

These valves have quickly changeable seats which are positioned

by the compressive force of the mating flanges.

The phenomenon of the

seat moving, due to water pressure on the upstream side of the seat when

the downstream flange was unbolted,

was unexpected.

The licensee is

performing (through the ACR process) root cause verification, as well as

the scope of and the need for procedural controls to ensure clearance

boundary adequacy in the future.

The inspectors will review the

corrective actions

adequacy

through routine

ACR

monitoring

and

evaluation.

Contamination Protection Practices

On February 10,

1991, the inspectors observed an individual inside the CV

who was not dressed in accordance with the applicable RWP requirements.

The individual was observed wearing a skull cap with her hair exposed;

the applicable RWP,90-637, required a cloth hood.

This condition was

reported to an onshift HP technician inside the CV who had the individual

correct her dress.

In addition, another worker was observed inside the

CV without his gloves taped to his PCs, which is considered a poor work

practice.

This was also reported to an HP technician who had the

individual tape the gloves.

These observations were later discussed with

the E & RC Manager who subsequently sent a memo to the HP Foremen

re-emphasizing the need for HP personnel to set and enforce high standards.

An NCV was issued in IR 90-18 involving failure of a laboratory technician

to dress in accordance with an RWP.

However, there is a dissimilarity

between the 90-18 item and the above RWP violation, in that the laboratory

technician failed to recognize that he needed protective clothing,

whereas,

the RWP violation involved improper dress.

The corrective

actions taken by the E & RC Manager before the end of the inspection

period were deemed appropriate. This violation is not being cited because

0

7

the criteria specified in section V.A of the NRC Enforcement Policy were

satisfied. This item is a NCV: Failure To Follow The Provisions Of A RWP

As Required By PLP-016, 91-01-01.

CV Cleanup

On January 31,

1991, while performing a general area inspection of the

CV,

the inspectors observed debris under two containment fan cooler

units.

The debris included a plastic bottle, two rolls of duct tape,

discarded gloves, a sign, metal tags,

and wads of paper and tape.

The

other two containment fan coolers were not examined.

The inspectors

observed isolated pieces of trash on, under, and behind various pieces of

equipment, panels,

and supports.

Upon exiting the CV, the inspectors

discussed the conditions with an SRO who had made a similar tour earlier

that day. The SRO had also observed the above conditions. These observa

tions were significant, in that, efforts had been in progress for a

minimum of three days to clean up the CV in preparation for restart.

The daily outage schedule for January 30 to January 31,

1991, listed the

final CV walkdown prior to 200 degrees and closeout per PLP-006, Contain

ment Vessel Inspection/Closeout, was to be at 2:00 p.m. on January 31. The

preliminary walkdown by the SRO on that day revealed that the final CV

closeout per PLP-006 was not possible. The resident inspectors also noted

that a partial CV walkdown by the licensee on January 29,

1991,

which

generated a list of 45 items to be addressed prior to CV closeout, had not

identified the debris under the containment fan coolers. The inspectors

discussed their observations with the Plant General Manager concerning

CV cleanliness.

The inspectors were concerned that these observations,

along with those documented in IR 90-05 and 90-12, indicated that the

cleanup inside the CV had not been approached in a thorough and systematic

manner.

Circuit Breaker Identification Aids

On January 18,

1991,

the inspectors observed that outdated circuit

breaker lists were posted inside instrument buss panels 7A and 9A.

The

circuit breaker lists provides information as to the function associated

with each circuit breaker located in a panel.

Subsequent review by both

the inspector and the licensee revealed that the problem also existed in

other instrument buss and power panels.

The method used to maintain

current circuit breaker lists in the panels involved a designated

operations technician receiving a controlled revision to the applicable

procedure containing the list.

He is then responsible for placement of

the revised list inside the panel.

However, in May 1990, the technician,

was inadvertantly deleted from distribution for these revisions.

At the

end of the report period, the current lists had been placed in the panels

and the procedure revision distribution list had been changed to include

the operations technician for distribution of future revisions.

One non-cited violation was identified.

8

3.

Installation And Testing Of Modifications (37828)

Modification M-1016, Electrical Penetration Replacement Testing

During performance of EST-048, Control Rod Drop Test (Refueling Outage),

revision 6, on January 29, 1991, the RPI for RCCA P-6 in control bank B

failed to increase in response to control bank B withdrawal.

However,

the RPI for RCCA D-10 in control bank C did increase in response to

control bank B withdrawal.

Similarly, when control bank C was withdrawn,

RCCA D-10 RPI failed to increase while RCCA P-6 RPI indication increased.

At that time, EST-048 was exited, all control rods were fully inserted,

the reactor trip breakers were opened,

and the rod drive cabinet fuses

were reinstalled.

ACR 91-060 was generated to document and investigate

this anomaly.

Upon investigation, it

was determined that the electrical penetration

through which these RPI cables traverse was changed from Penetration C-2

to E-1 during implementation of modification M-1016, Electrical Penetra

tion Replacement.

The modification had been declared operable on

January 22, 1991. Apparently, during or after modification implementation

the RPI cables for P-6 and D-10 (cable numbers C2078BN and C2079BC,

respectively) were "rolled" or switched. This situation was not detected

during modification implementation,

QC verification, or modification

acceptance testing.

As a result of the modification being declared operable without detection

of the problem,

the adequacy of the acceptance tests specified and

performed was evaluated.

In the case of the RPI cables, the acceptance

test specified was the performance of loop calibration procedure LP-551,

Rod Position Indication System, revision 3. The test was to be performed

in 45 relocated cables. After the rolled leads were corrected, LP-551 was

not performed as expected. Upon further investigation it was determined

that LP-551 had not been performed as required for any of the 45 RPI

cables prior to the modification being declared operable. The maintenance

technicians had initialed the functional test signature blocks as having

been performed, when evidently, the only test performed was a resistance

check of each RPI's cable.

The resistance check could not and did not

identify the rolled leads.

Additionally, the functional tests (LP-251,

Radiation Area Monitors RMS R1-R8) specified for radiation monitors R-2

and R-7 were signed as having been completed. However, this procedure had

been deleted approximately two months earlier and replaced by test

procedure

OST-924,

Radiation Monitoring

System,

neither of which

was performed for the acceptance test. The testing which the technicians

performed cannot be verified.

In addition, there are other examples

within the modification where the testing performed was not the specific

testing specified. The failure of the maintenance technicians to conduct

the functional testing specified in the modification is the first example

of a violation:

Activities Affecting Quality Were Not Performed In

accordance With Procedures And Drawings, 91-01-02.

9

During the review of the testing conducted versus the testing specified

to be performed, it was identified that some functional tests specified in

the modification were not adequate to test the components/cables which

were affected by the penetration replacements. Examples of this included

a specified resistance check as a functional test on approximately 60

temperature elements. The resistance checks performed only verified the

equipment was connected; the tests did not confirm that the resistance

was in fact, at the instrument it should be.

Additionally, LP-551, which

was the functional test specified for the RPIs,

was inadequate to

functionally test individual RPIs.

As such, if the rolled leads were not

identified during performance of a test (EST-048)

unrelated to the modi

fication, these RPI would not have been functionally tested.

There were

additional tests specified in the modification, the adequacy of which were

questionable.

Examples of these questionable tests included PIC-009,

Current/Pressure (I/P) Transducer,

and PIC-401, Valve Positioner, which

were specified as the functional tests for three valves; and OP-202,

Safety Injection and Containment Vessel Spray System,

which only

performs a valve line-up for valve HCV-936.

The failure to adequately

establish tests is a violation: Modification M-1016 Acceptance Tests were

Inadequate, 90-01-03.

There are two concerns associated with these violations.

The first

relates to the inadequate acceptance tests, in that there appeared to be

inadequate reviews performed on the tests' adequacy during the modifica

tion review and approval process.

Modification acceptance testing

adequacy has

been a previous identified concern and this problem

underscores the need for additional efforts in this area.

The second

concern relates to the oversight provided during component/cable functional

testing, in that, the modification was declared operable without the

functional tests specified being performed.

This testing was performed

over a period of several weeks, thus allowing numerous occasions for the

identification of the tests not being performed as specified.

More

interactive oversight may be warranted during modification development,

implementation, and testing.

Two violations were identified.

4. Monthly Surveillance Observation (61726)

The inspectors observed certain safety-related surveillance activities on

systems and components to ascertain that these activities were conducted

in accordance with license requirements.

For the surveillance test

procedures listed below, the inspectors determined that precautions and

LC~s were adhered to, the required administrative approvals and tagouts

were obtained prior to test initiation, testing was accomplished by

qualified personnel in accordance with an approved test procedure, test

instrumentation was properly calibrated, the tests were completed at the

required frequency,

and that the tests conformed to TS requirements.

10

Upon test completion, the inspectors verified the recorded test data was

complete,

accurate,

and met TS requirements; test discrepancies were

properly documented and rectified; and that the systems were properly

returned to service.

Specifically, the inspectors witnessed/reviewed

portions of the following test activities:

EST-004

Isolation Valve Seal Water

EST-006

Containment Spray Nozzles

EST-049

Rod Drive Mechanism Operation Testing

(Refueling Outage)

EST-058

SI-890A And 890B Check Valve Test

OST-163

Safety Injection Test And Emergency

Diesel Generator Auto Start On Loss Of

Power And

Safety

Injection And

Emergency Diesel Trips Defeat

OST-351

Containment Spray System

SP-1002

RHR Pump Flow Test

SP-1007

RHR Pump Flow Test

SP-1010

Service Water Flow Test

SP-1012

Control Rod Drive Mechanism C-07

Testing

OST-351

On January 17, 1991, the inspectors witnessed the performance of OST-351,

Containment Spray System, revision 9.

The test was terminated when

certain relays were not energized as required by OST steps 7.2.13 through

7.2.16.

A review of Safeguards System drawings CP-380-5379-3233,

3235,

and

CWD B-190628 sheets 141,

144,

and 147,

indicated that the relays

should not have been energized. A previously performed step, 7.2.9, had

returned the bistables, which were tripped to cause a containment spray

initiation, to their normal position.

This action reset the indication

signal and removed the power from the relay coils which were to be

verified as energized in steps 7.2.13 through 7.2.16.

It was also

observed that steps 7.2.13, 7.2.14, and 7.2.15 referred to the relays as

SX relays on panels AA,

KA,

and MA, where as the CWD sheets 141,

144, and

147 referred to these relays as SX1, SX2, and SX2 on panels AA, KA, and

MA, respectively. Review of OST-351, revisions 6 and 7, completed May 28,

1987,

and November 15, 1988, respectively, as well as revision 8 (never

performed) revealed these earlier revisions also contained the step to

reset the bistables to normal prior to performing the relay verification

steps.

Thus, on at least two prior occasions, the procedure steps were

improperly signed as having been satisfactorily completed.

Apparently,

personnel preparing the procedure knew that the steps were to be performed

in response to the containment spray initiation signal and not in the

sequence specified in the procedure (i.e., after the initiation signal

was reset.

Personnel implementing the procedure had performed the steps

as intended, not as written. The fact that on January 17, 1991, I & C

technicians did not sign OST-351 steps 7.2.13 through 7.2.16 as being

satisfactorily completed,

indicated that in the Maintenance unit an

evolving awareness of what constitutes procedure adherence is occurring.

At the same time, however, a licensed operator signed that "both contain

ment spray pumps START"

and selected valves "have OPENED"

and "have

CLOSED" after the containment spray initiation signal was reset.

Since

the steps did not require verification that the pumps remain running or

the valves remain opened or closed; the operator had actually acknowledged

that the actions occurred as a result of the initiation signal reset

verses the initiation signal.

The failure by the operator to recognize

that changes of state of equipment during testing should be attributed to

the step immediately preceding the change of state, unless otherwise

specified, was identified as a weakness in procedure adherence. This was

discussed with the Operations Manager.

On January 18, 1991, OST-351 revision 10, was issued to correct the above

problem (i.e., the actions which occur as a result of the initiation

signal are to be verified prior to resetting the initiation signal).

Revision 10 incorporated additional steps to correct another deficiency

(i.e., the B train MSIV closing solenoid circuits were not being completely

tested).

To address this oversight, revision 10 included steps to verify

that relays SX2, SX1 and SX1 on respective panels JB, FB, and DB energize.

However, with the RTGB control switch in the shut position (the condition

it

would most likely be in due to these steps routinely being performed

when the MSIVs are under clearance) these relays are already energized

and remain energized.

This was recognized by the onshift personnel

preparing to perform the new revision.

Revision 10 was satisfactorily

performed on January 19,

1991, with the notation that relays on panels

JB, FB, and DB are always energized with the control switches in the shut

position. Abnormal Condition Report ACR 91-035 was issued to address the

adequacy of OST-351 to test the MSIV isolation logic.

Revision 11 was

issued and was successfully performed on January 26, 1991, to completely

test the MSIV logic.

The failure to provide adequate steps in revision

10 to test the MSIV logic indicated a weakness in the preparation and

technical review process involved with logic test procedures. Discussion

with the revision 10 procedure preparer revealed that he had only received

on-the-job training involving preparation of, or changes to logic test

12

procedures.

The inadequacy of OST-351 revision 10 to completely test the

MSIV closure logic is a violation:

OST-351, Revision 10 Was Inadequate

In That It Did Not Completely Test The MSIV Logic, 91-01-04.

Another example of a recently issued inadequate procedure change was

temporary change no. 4092 issued to SPP-011, Removal And Restoration Of

SI Actuation.

The temporary change dated January 17,1991, incorporated

steps for a continuity check to be used to verify proper wiring restora

tion.

The steps would not work as written because an indicating light

circuit was in parallel to the circuit being verified.

Another temporary

change dated January 26,

1991,

to SPP-011 was issued and successfully

performed to verify continuity of the restored wiring.

Revision 5 to

SPP-011 was issued on February 16,

1991, to permanently incorporate this

change into the procedure.

Service Water System Flow Test

On January 29,

1991,

a SW system flow test was conducted per SP-1010,

Service Water Flow Test.

The SW system had undergone extensive

repairs/refurbishment and this test was performed to confirm adequate

system performance. The system mode tested was an accident configuration

(i.e.,

two SW pumps running, turbine building SW loads isolated, and

approximately 10,000 gpm circulated through the CCW HXs).

The test

verified that the minimum required SW flow of 564 gpm to each EDG HX

was satisfied.

The flows to the EDG HXs were acceptable and exceeded the

required 564 gpm with and/or without the SWBPs operating (with the SWBPs

operating, the EDG HXs receive less flow).

The KYPIPE computer program

was used to model system configurations and expected resultant flows and

pressures.

The KYPIPE predictied flows and pressures corresponded

similarly with those measured during the test.

Drawing Deficiencies

During review of the OST-351 deficiencies discussed above, the licensee

and the inspectors together identified that logic drawing CP-300

5379-2759,

revision 15,

did not show that a high high containment

pressure containment spray initiation signal would initiate an SI signal

if

RCS coolant temperature is above the low TAVG setpoint.

Safeguard

drawings CP-380-

5379-3232,

3233 and 3235 show that the automatic

containment spray initiation relays AS1 and AS2 energize relays SL1 and

SL2 which energize the safety injection initiation relays SIA1 and SIA2.

This is apparently a backup to the high containment pressure SI

initiation signal.

The inspectors also identified two other drawing discrepancies.

Reactor

Protection System drawing CP-380 5379-3244 revision 12,

showed the

reactor trip contacts in the reactor trip trains A and B being powered

from 125 VDC panel A circuit 10 and panel B circuit 9, respectively.

13

However, drawing CP-380 5379-3243 and 3252 show that the trip contacts

are powered from panel A circuit 18 and panel B circuit 18 via train A

and B terminal strips 5T7.

The licensee has agreed that drawing 3244 is

in error and will revise it. Residual Heat Removal System Flow Diagram

5379-1484 revision 19, did not show that the piping to valve RHR-744A,

the SI Cold Injection Valve, is reduced from 12 to 10 inches. A 12 X 10

inch reducer is shown upstream of the RHR-744B valve.

The licensee is

reviewing this drawing to determine if it should be clarified.

One violation was identified.

5. Monthly Maintenance Observation (62703)

The inspectors observed safety-related maintenance activities on systems

and components to ascertain that these activities were conducted in

accordance with TS,

approved procedures,

and appropriate industry codes

and standards.

The inspectors determined that these activities did not

violate LCOs and that required redundant components were operable. The

inspectors verified that required administrative, material,

testing,

radiological,

and fire prevention controls were adhered to.

In

particular, the inspectors observed/reviewed the following maintenance

activities:

SP-1008

Removing Green Oily Resin And

Replacing Power Wiring In MCCs 5,6,

9, & 10

SP-1015

Secondary Source Inspection And

Recovery

SP-1016

Testing And Latching, Inspection And

Unlatching Of The RCCA At Core

Location C-07

SPP-011

Removal And Restoration Of SI

Actuation

WR/JO 91-ACDK1

Reactor Head Stud Cleaning

Machine Tool Wire

On January 4, 1991,

the B main feedwater stop valve V2-6B,

failed to

close.

Upon investigation poor continuity readings were measured on one

phase of the MCC closing contactor and a clear covering, like nail polish,

was popped off the contact surface.

The valve subsequently cycled

properly. A similar incident involving the need to clean an unidentified

substance from contactors associated with V2-35B, radiation monitor sample

for HVH-2 return isolation valve, had occurred during the preceding week.

14

In neither instance was the removed material retrieved for analysis.

Inspections revealed a green liquid gel in the contactor housings,

but

not on the contact surfaces.

Examination of other 208 and 480V MCCs

revealed that most compartments exhibited green liquid migration out of

the power conducting internal wiring of the MCCs.

Initial evaluation revealed that the green liquid appeared to be a

vegetable oil plasticizer used in the PVC covered wire. The wire was black

in color and marked as machine tool wire -

105 degrees C.

Subsequent

analysis indicated that the green liquescent material is a conductor when

in a liquid/gel form but may be a conductor or insulator when dried;

dependent upon the amount of copper oxide salts dissolved in the material.

The liquid may range in color from light green (almost clear in thin

films) to dark green, also depending on the amount of dissolved copper

oxide salts.

The licensee determined that the above mentioned valve

failures were most likely due to the plasticizer migrating onto one or

more of the contactor contacts.

The licensee's inspection of Class

1E MCC

compartments revealed the

presence of the green material in most compartments.

The only use

identified for machine tool wire was to connect the breaker to the

contactors.

The effected MCC compartments are size 1 compartments

manufactured by Westinghouse around 1962.

The wire is commercial grade

AWG #12 wire supplied under industry standards in effect at that time.

Westinghouse obtained wiring from several different vendors during the

early 1960s.

Records review to date has not identified the manufacturer

or manufacturers of the machine tool wire. In the late 1960s, Westinghouse

discontinued use of this wire and began use of wire with a different

insulating material.

The licensee developed and implemented SP-1005 to replace the machine

tool wire with surprenant wire and cable type CL-1251 XLPE 600V wire and

to clean the contactors in 111 compartments of MCCs 5, 6, 9, and 10.

Since the green material was also observed in non-safety related MCCs,

plans were being developed to replace the machine tool wire and clean

these affected compartments during RO 14.

The inspectors verified via

examination of all compartments on MCC 6 and 9, that the wire was not used

in other applications.

The inspectors also looked inside reactor protec

tion and safeguard cabinets and instrument buss and power panels. Again,

no other use of the wire was discovered.

Fuse Control

On January 16,

1991,

while witnessing performance of OST-163,

the

inspectors observed that the installed A SI pump control power fuse was a

Bussman Type F61C 30 AS fuse. The similar fuse associated with C SI pump

was a Bussman F61C 10 AS fuse.

Control wiring diagram B-190628 sheets

237, revision 14, and 239, revision 12, required 10 ampere fuses to be

15

installed in the A and C SI pump 125 VDC control circuits respectively.

The licensee verified that the fuse installed in the A SI pump circuit

was a 30 ampere fuse. Since there were no replacement 10 ampere fuses in

stock, the fuse from the C SI pump circuit was placed in the A SI pump

circuit.

The C SI

pump has been offsite for casing repairs since

mid-1989.

Procedure OST-163 was subsequently successfully performed,

thus ensuring the circuit would perform correctly with the lower ampere

fuse installed.

The inspectors verified that the correct fuse size was

installed in six other randomly chosen emergency buss El and E2 breaker

control circuits. Other discrepancies were not identified. The licensee

has subsequently verified that other fuses installed in El and E2 breaker

control circuits are in accordance with the CWDs.

Failure to have the

size fuse specified on the CWD installed is a second example of violation

91-01-02.

The inspectors also noted that numerous CWDs did not specify fuse sizes.

Furthermore,

few safety-related CWDs specify a specific kind or type of

fuse.

A fuse schedule which provides sizes, acceptable types,

and

manufacturers for fuse applications did not exist. The licensee has been

controlling fuses by replacement-in-kind or by engineering evaluations if

a replacement-in-kind fuse was unavailable.

However, design information

involving what fuse attributes are taken credit for in circuit protection

or coordination are not always available.

Some circuits such as those

associated with Appendix R coordination

have design calculations

available.

The licensee was developing a fuse control program to address

these issues. The present status of the licensee's effort include:

o

Design guide for fuse selection criteria was in draft

o

Identification of calculations which need to be performed to support

coordination and/or protection should be completed by Spring 1991.

Scheduling of presently identified calculations was in progress

o

A fuse schedule which will provide acceptable size, types,

and

manufacturers for each application was being planned.

An initial

fuse schedule with known, verified information for most DC fuses and

some AC fuses was planned to be issued this fall

The above three items are considered an IFI: Review Fuse Control Program

Development And Implementation, 91-01-05.

DC Fuses

Concerns were raised at the Harris Nuclear Plant involving possible

misapplication of fuses in DC circuits.

The concerns involve applying

voltage and interrupting current ratings of either AC fuses to DC

circuits or

DC fuses to higher than specified DC voltages without

16

consulting the manufacturer.

On January 25 and 26,

1991,

a licensee

field walkdown identified the manufacturer and type of approximately 350

fuses installed in primary 125 VDC circuits.

Engineering calculations were performed to identify the maximum fault

current available for each fuse type at the pertinent sections of the 125

VDC distribution system.

The fuse types, ratings,

and maximum fault

currents were submitted to the manufacturers for evaluation. As a result

of this process, eleven circuits were identified for which the existing

fuses were replaced. The functions associated with these circuits are:

o

Batteries A and B DC MCCs undervoltage monitoring (2 circuits)

"

PZR safety valve flow monitoring (2 circuits)

o

Condensate pump B and Feedwater pumps A and B ERFIS status (3

circuits)

o

HVH-1,2,3, and 4 vibration and flow monitoring (4 circuits)

The HVH vibration and flow monitoring circuits had 32 V fuses installed

in 125 VDC applications.

The other fuses contained in the above circuits

were suspect per the vendor as a result of the concerns raised at the

Harris Nuclear Plant.

Engineering evaluation EE 91-030 indicated that the inspection, while

not a complete inspection, did represent the majority of DC fuses

installed.

Based upon the limited number of problems identified, EE 91-030 concluded that additional fuse inspections, necessary to complete

a DC fuse list, could be performed as plant conditions permit and are not

required prior to startup from RO 13.

The licensee presently plans to complete inspection of the installed DC

fuses by the end of RO 14.

This information will be incorporated into

the fuse schedule being developed as one element of the fuse control

program discussed above.

MCC Inspection

During Class 1E MCCs 6 and 9 compartment inspection, the inspectors

observed various abnormal conditions.

These included: V-749B compartment

thermal overload reset button was missing and control power transformer

was bolted on the same side, thereby allowing the transformer to move on

its attachment bracket; SI-845B compartment bucket top latching mechanism

was open; V6-33C,

V6-33D,

V6-33F,

V6-35B,

V6-35D,

V2-16C

and V-749B

compartments had one or both bucket bottom alignment/attachment screws

not engaged; and V2-20A control power circuit contained a Bussman BAF 3

fuse.

The inspectors observed that V2-20B compartment contained a

17

Bussman BAF 1 fuse.

The licensee was informed of these conditions. The

licensee determined that either the 1 or 3 ampere fuse size was

acceptable for the application; however, for consistency, the fuses will

be changed so that the same size will be used for similar applications.

A second example of a violation was identified.

6. Onsite Review Committee (40500)

The inspectors evaluated certain activities of the PNSC to determine

whether the onsite review functions were conducted in accordance with TS

and other regulatory requirements.

In particular, the inspectors

attended

PNSC meetings on January 30 and February 7, 1991, involving

plant status review prior to exceeding 200 degrees and a procedure change

to allow head lift

under existing plant equipment conditions,

respectively. It was ascertained that provisions of the TS dealing with

membership, review process, frequency, and qualifications were satisfied.

No violations or deviations were identified.

7. Followup (92709, 92701, 92702)

(Closed) LER 88-07, HVH-2 Breaker Failed To Close On Safeguard Sequence

During Performance Of Special Test.

On February 12,

1988, during

performance of a special test while in cold shutdown, containment fan

cooler HVH-2 failed to start during the safeguards sequence.

Licensee

investigation revealed that the breaker, a Westinghouse model DB-50, did

not close because of a faulty alarm switch located in the closing circuit

of the breaker.

Apparently, oxidation buildup on the alarm switch

contacts was the root cause of the breaker not closing.

The licensee

subsequently checked alarm switches on other emergency switchgear supply

breakers, and found 11 additional switches that had intermittently high

contact resistance readings.

These switches were replaced.

Interviews

with the Manager-Electrical Systems (Technical Support) indicated that

the preventative maintenance procedure for DB-50 breakers,

PM-402

revision 5, Circuit Breaker Inspection and Testing, requires the alarm

switches to be replaced every fifth refueling outage.

Furthermore, the

inspector was informed that alarm switches which had not been replaced

todate will be replaced during the next refueling outage, and PM-402 will

be revised accordingly.

In addition, the licensee contacted the vendor

regarding testing the alarm switches.

The vendor indicated that there

was not a criteria for such a test, and alarm switch failures were not a

widespread problem. A successfully cycling of the breaker, as is done

during maintenance and surveillance testing of associated equipment, is

the best functional test of the alarm switches. This item is closed.

(Closed)

LER 88-08, Operation In Violation Of Technical Specifications

Due To Analytic Input Error. This issue involved an error in fuel cycle

12 analytic factor decks used to process in-core detector measurements

18

and to monitor compliance with TS

thermal-peaking limits.

ANF

Corporation notified the licensee (NFS)

of the error (assignment of

incorrect isotopic data to a reinsert assembly) on March 24, 1988. Flux

map reevaluations using corrected analytic factor decks indicated that

allowable power level while operating with a 5 percent delta flux target

band should have been 99.98 percent instead of the 100.22 percent

originally calculated.

To ensure peaking factor conformance,

TS 3.10.2.2.2 requires the use of the APDMS when power levels exceed the

allowable power level.

Consequently,

subsequent review identified

operations during June 29 through August 12,

1987, as being nonconserva

tive (i.e., delta flux target band greater than 3 percent and APDMS was

not in use).

However,

because of inherent conservatism in ANF's power

distribution control methodology (PDC-II), subsequent analysis was able to

demonstrate that the plant did not operate in an unsafe condition.

The

inspector considers the

additional in-core deck checkout reviews now

being conducted by NFS,

as well as those actions taken by ANF to

strengthen related internal performance and activities to be appropriate.

Somewhat related, the inspector notes that IR 90-23 addressed an ANF LOCA

computer code error which was reported by the licensee on October 23,

1990.

Consequently, generic ANF concerns will be addressed during the

followup of this more recent event under URI 90-23-01.

LER 88-08 is

considered closed.

(Closed)

LER 88-19, Inoperable Containment Fan Coolers Due to Biological

Fouling.

On September 5, 1988,

the licensee notified the NRC of a

four-hour non-emergency event due to inoperable containment fan coolers.

The licensee found that a significant amount of biological fouling had

taken place in the cooling coil tubes.

The fouling resulted in the tube

inner diameter being reduced and caused the heat removal capability of

the coolers to be reduced under Design Basis Accident conditions.

The

licensee also found that the four fan motor coolers were also fouled in a

similar manner.

Immediate corrective actions included cleaning out the

heat exchangers, inspection of the tubes, and hydrostatic testing of the

tubes.

An assessment of the event and a root-cause evaluation determined

that due to lack of a performance monitoring program and lack of flow

(during the long steam generator outage in 1984) the tubes became fouled.

To prevent recurrence, the licensee implemented plant modification M-968

which installed RTDs and differential pressure instruments as performance

monitoring instrumentation on HVH-4.

The instrumentation allows HVH-4

performance to be monitored, thereby providing detection capability for

potential degradation of equipment due to biofouling.

A side-stream

monitor was also installed to allow for close monitoring and observation

of biological growth inside piping and coolers.

Additionally, a

chlorination process was installed to treat the entire service water

system to help prevent biofouling.

Instrumentation similar to that

installed on HVH-4 were installed on HVH-1,

2, and 3, during RO 13.

Inspections of two

HVH units,

performed during RO

13, revealed no

19

evidence of biofouling.

Based on over two years of successful operation

the licensee's long-term corrective actions have proven effective in

preventing biofouling of the HVH units and associated motor coolers.

This item is closed.

(Closed)

LER 88-26,

Inadvertent Safeguards Actuation.

On November 14,

1988, the plant was in cold shutdown for refueling when a safeguards

actuation was received from an inadvertent SI signal.

The licensee's

investigation revealed that the pressurizer SI block permissive was

removed when licensee staff de-energized two of three reactor protection

channels as part of a plant modification.

This safeguard actuation did

not result in an actual injection into the reactor coolant system; the

breakers to the safety injection pumps were open and the discharge valves

were closed and de-energized.

Remaining safeguards equipment functioned

as designed.

The licensee's root cause investigation indicated that

there were inadequate procedural precautions to ensure that safeguards be

de-energized prior to removing two of three reactor protection channels.

In addition, the licensee indicated that there was some miscommunication

between the operations coordinator and the clearance center operators, in

that, only a partial breaker lineup was required, yet a full breaker

lineup was initiated resulting in the inadvertent Safeguards actuation.

The intended partial breaker lineup would have prevented the inadvertent

SI signal.

Corrective actions included discussions between licensee

staff, revisions to applicable procedures, and the placement of operator

aids in the control room and on the DC breakers which supply the

Safeguards System.

The inspector held discussions with operations

personnel,

reviewed OST-163 revision 15,

Safety Injection Test,

and

Emergency Diesel Generator Auto-Start on Loss of Power and Safety

Injection and Emergency Diesel Trips Defeat (Refueling), and viewed the

operator aids.

At the time of the inspection, there were no inadvertent

SI actuations since the one reported in the subject LER. The corrective

actions taken by the licensee were deemed adequate by the inspector.

This item is closed.

(Closed)

LER 89-01, Hydrogen Introduced Into The Instrument Air System.

This event is addressed in this section under the closure of URI 88-38-02.

(Closed)

LER 89-02, Failure OF Fast Response RTD Thermowells.

This item

was not required to be reported per 10 CFR 50.73.

However, a voluntary

LER was filed because the event could be of interest to the industry and

the NRC.

Followup inspection is being tracked as IFI 89-07-02.

Hence,

because the LER is redundant to IFI 89-07-02,

the LER is considered

closed.

(Closed) LER 89-03, Licensee-Identified Violation Of 10 CFR 20.101 Due To

Incomplete Contract Employee Forms NRC-4. The subject item was inspected

and closed in IR 89-28 as IFI 89-FRP-01.

20

(Closed) LER 89-06, Reactor Trip Due To Loss Of Turbine E-H Control Power

Supplies.

Prior to restart from the reactor trip the inspectors verified

that equipment repairs and protective circuitry setting adjustments were

completed as described in the LER.

During RO 13, Modification M-1046,

Replacement of E-H Power Supplies, was installed to replace the original

equipment.

Originally, electronics for the EHC system were powered from

two power supplies.

Each power supply provided -15 VDC, +15 VDC, and +48

VDC.

The modification replaced each unit with three individual power

supplies, one for each voltage requirement.

This new configuration

eliminated the cascading failure mode which initiated the reactor trip.

With installation of M-1046, the corrective actions described in the LER

has been completed. This item is closed.

(Closed)

LER 89-08, Potential Loss Of Residual Heat Removal Capability

Due To Pump Flooding.

Inspection Report 89-09,

dated June 26,

1989,

issued an NOV involving this matter.

Followup of LER 89-08 will be

incorporated into the inspection of the VIO, 89-09-05, hence LER 89-08 is

considered closed.

(Closed)

LER 90-11, Technical Specification Violation Due To Inoperable

Fire Barrier Penetration (Fire Damper).

The licensee was unable to

determine when or how the fire damper was mispositioned. The inspectors

verified that the corrective action specified in the LER had been

completed.

This action was to place a permanent label on the damper

access door to inform personnel that the damper is to remain closed.

The

label reads "STOP Damper 77 is a closed damper -

Do not open 77".

This

should preclude future inadvertent opening. This item is closed.

(Closed)

IFI 88-03-03, Subcooling Margin.

The subject item concerned

failure to establish a basis for deviating from the recommended values in

the WOG ERG when end path procedures were developed. Subsequently, a EOP

inspection identified this as a general concern involving not only this

specific item, but numerous other examples.

This general concern was

identified as IFI 89-16-01.

Followup of IFI 88-03-03 disclosed that a

calculated basis for the deviation was still scheduled to be performed. A

statement was contained in the generic analysis applicability document,

dated October 29, 1990, which indicated the values used were bound by the

generic documents.

However, not having the calculation performed to

support the values used in the procedures and not having this documented

in the setpoint document by September 28,

1990, was a failure to meet a

commitment identified in the Response To NRC Inspection Report No.

50-261/89-16 dated December 8, 1989. The licensee has agreed to submit a

revised response providing a date when this calculation and others which

may not yet be completed, will be completed and incorporated into the

setpoint document part of the PSTG.

Followup will be performed under

IFI 89-16-01, hence the subject item is closed.

(Closed) IFI 88-06-01, Review Inadvertent Shipment Of Contaminated Liquid

To Quadrex.

On February 24, 1988, the licensee made a shipment of two

Sea/Land containers to the Quadrex Recycle Center in Oak Ridge,

21

Tennessee.

Although the shipping papers identified the physical form of

the enclosed material as being a solid, approximately nine gallons of

liquid had unknowingly been shipped.

This issue was subsequently

reviewed by a regional radiation specialist and violation 88-28-10 was

identified for failure to indicate proper physical form of material on

shipping papers.

As this was a violation of minor safety/environmental

concern for which adequate corrective actions had been taken, it was both

cited and closed in IR 88-28.

Consequently, IFI 88-06-01 is also

considered closed.

(Closed)

IFI 88-28-05,

Licensee To Develop Methodology To Detect

Biological Growth in HVH 1-4. The licensee has installed a computer-based

fouling monitoring system which monitors the heat transfer resistance and

fluid frictional resistance in a section of tubing which is representative

(size and alloy composition) of the tubing in the HVH units.

If fouling

should occur, both heat transfer resistance and fluid frictional resistance

should rise.

The inspector conducted interviews with the HVAC and SW

system engineers who indicated that the fouling monitor system, while not

calibrated against traceable standards,

does provide an indication of

biofouling. This was validated during RO 13 when the section of tubing

was cleaned and reinstalled.

Original data was then compared to data

obtained after the test section was cleaned.

This data indicated that

there was a slight positive change following cleaning, which indicated

that some fouling had taken place in the two years the test section was

interposed in the SW sidestream. However, visual examination of the test

section revealed fouling was not evident.

In addition to sidestream

monitor,

the licensee has implemented

SW chlorination,

and monthly

performs EST-102,

Performance Testing of HVH-4 Reactor Containment Fan

Cooling Unit.

The licensee considers this test to be representative of

the other three HVH units.

Instrumentation installed during RO 13 on the

HVH-1, 2, and 3 will enable the licensee to perform performance testing on

these HVH units.

The licensee is revising EST-102 to incorporate this

change.

At the time of the inspection, no unsatisfactory results have

been obtained.

In addition, inspection performed of two HVH units

revealed no fouled tubes.

This item is closed.

(Closed)

IFI 88-38-03,

Review Selection Methodology,

Adjustment,

And

Testing Of M-939 Breaker Setpoints.

The subject modification (M-939)

involved the replacement of MCPs in safety-related MCCs 5,6,9, and 10 in

order to correct coordination problems.

As discussed in IR 88-38, the

MCPs being installed under M-939 were experiencing trip setpoint anomalies,

requiring substantial adjustment from their calculated setpoints.

Investigation into the matter determined that unrecognized limitations in

the Westinghouse MCP setpoint application guide and personnel errors

during preparation/review of M-939,

resulted in an inadequate margin

between locked rotor current and the MCP setpoint. Accordingly, more than

20 MCPs required upgrading to a larger size and approximately 120 required

new setpoints. The inspector reviewed the completed modification package,

including the design change notices (DCNs 939-19,

21, 22, and 24) which

22

accomplished said rework, and verified the MCPs were subsequently tested

prior to plant heatup above 200 degrees F. Actions taken with respect to

identified casual factors (addressed in both SCR 89-07 and NCR 89-05)

were also reviewed and found to be appropriate. This item is closed.

(Open)

IFI 89-16-01,

Develop A New PSTG.

During inspection of IFI

88-03-03, the inspectors observed that IFI 89-16-01 had been considered

as satisfactorily completed by the licensee and was listed as closed in

the regulatory action item tracking system.

The inspectors were

concerned about the circumstances surrounding closure of IFI 89-16-01

when prior to this closure, outstanding work had been identified which

was to be incorporated into the setpoint portion of the PSTG.

This item

remains open as described in closeout of IFI 88-03-03.

(Closed) IFI 88-28-01, Establish of EQ Lifetimes Inside CV Based Upon

Actual

Temperature Conditions.

Temperatures

used to calculate EQ

lifetime of equipment in the CV were based on bulk average temperature in

the CV.

There were concerns that this bulk average temperature was not

representative of actual temperatures in the immediate vicinity of EQ

equipment.

Procedure SP-797,

Special Procedure for Monitoring CV

Temperature,

was performed to define the CV temperature profile.

The

actual temperatures inside the pressurizer cubicle were much higher than

the bulk average temperature in the CV.

As a result, the qualification

lifetimes of EQ limit switches and solenoid valves were exceeded.

The

licensee has implemented a satisfactory PM schedule to change these

components. This item is closed.

(Closed) URI 88-28-06, Review LER 88-21 And CV Operability Requirements

After Opening Of CV Purge Exhaust Valves. This item concerned the events

associated with the September 22,

1988 reactor shutdown which was

prompted by leaking CV purge exhaust valves V12-8 and V12-9.

The cause

of the leakage,

subsequent inspection/repair activities, and related

corrective actions were adequately addressed in LER 88-21, which was

closed in IR 90-12.

With regard to operability requirements,

the TS

requires valves V12-8

and V12-9 to be closed whenever containment

integrity is required except when purging for safety-related reasons.

Accordingly,

by design the valves will automatically open/shut upon

initiation/securing containment purge fans. To verify system alignment

control,

the inspector reviewed OP-923,

Containment Integrity,

and

OP-912,

Penetration Pressurization System.

From this review,

it

was

confirmed that whenever containment integrity is required,

OP-923

requires valves V12-8 and V12-9 to be operable (i.e.,

capable of

automatic closure) and OP-912 requires the valves' associated PPS header

to be in service.

Furthermore, OP-912 specifies that PPS header pressure

must be maintained above 42 psig or hot shut down must be achieved within

8 hours9.259259e-5 days <br />0.00222 hours <br />1.322751e-5 weeks <br />3.044e-6 months <br />, followed by cold shutdown within the next 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />.

To assure

proper air pressurization occurs between the valves once a CV purge is

23

secured, section 8.1 of OP-921,

Containment Air Handling, requires PPS

header pressure to be specifically verified. Consequently, the inspector

had no further concerns. This item is closed.

(Closed)

URI 88-28-08, Followup On Actions To Address Equipment Affected

By An Increased CV Submergence Level.

This item was also the subject of

LER 88-022 and supplement 1 to LER 88-022.

The LER was inspected and

closed in IR 89-26.

During this review, the inspector questioned the

qualification of repairs made to penetration F-011 cables.

These items

are being tracked as URI 89-26-02 and 89-26-03.

Thus, URI 88-28-08 is

redundant to these items, and is considered closed.

(Closed)

URI 88-38-02,

Review Hydrogen Event Report, Associated Root

Cause And Corrective Actions.

This item concerned the intrusion of

flammable concentrations of hydrogen into station and instrument air

systems due to personnel error while conducting a main generator air

tightness test on January 6 -

7, 1989.

Specifically, personnel

performing the test inadvertently cross connected plant air systems to

the hydrogen supply for the main generator's cooling system.

Considering

the potential impact this test had on safety-related systems and the fact

that it

was being accomplished without a written procedure, a violation

was issued accordingly on April 6, 1989

(EA

89-02).

The licensee's

corrective actions (addressed in the May 8, 1989 response to the

violation and

LER 89-01)

included:

(1) revising OP-507,

Generator

Hydrogen System, to provide written instructions for conducting a main

generator air tightness test and to ensure proper clearance on the bulk

hydrogen supply; and (2) revising OMM-005, Clearance and Test Request, to

specifically set the bounds on what actions can be taken within a

clearance boundary, as well as delineating how the introduction of fluids

(gas

or liquid) and

system restoration is to be accomplished by

Operations.

Based on a review of the implemented procedure revisions, as

well as,

the Main Generator Air Test Procedure (Section 8.6 of OP-507)

which was successfully completed in December 1990, corrective actions are

considered appropriate to preclude recurrence of this event.

This item

is closed.

(Closed) VIO 89-03-02, Restoration Lineup Of OST-163 Results In BIT Inlet

Valve Being In A Position Other Than That Established For OST-162.

The

inspectors reviewed the licensee's response dated May 5, 1989, to the

NOV.

The inspector verified that OST-162 and OST-163 was revised prior

to their performance during RO 13 as committed.

The revision involved

combining OST 162 and OST-163 into one procedure designated as OST-163.

This corrective action is considered adequate to preclude repetition.

This item is closed.

No violations or deviations were identified.

24

8. Exit Interview (30703)

The inspection scope and findings were summarized on February 25,

1991,

with those persons indicated in paragraph 1.

The inspectors described

the areas inspected and discussed in detail the inspection findings

listed below and in the summary.

Dissenting comments were not received

from the licensee.

Proprietary information is not contained in this

report.

Item Number

Description/Reference Paragraph

91-01-01

NCV -

Failure To Follow The Provisions

Of A RWP As Required By PLP-016

(paragraph 2)

91-01-02

VIO - Activities Affecting Quality

Were Not Performed In Accordance With

Procedures And Drawings In That

Modification Testing Was Not Performed

AS Specified And An Incorrect Sized

Fuse Was Installed (pragraphs 3 and 5)

9 1-01-03

VIO - Modification M-1016 Acceptance

Tests Were Inadequate (paragraph 3)

91-01-04

VIO -

OST-351 Revision 10 Was

Inadequte In That It Did

Not

Completely Test The MSIV Logic

(paragraph 4)

91-01-05

IFI - Review Fuse Control Program

Development

And

Implementation

(paragraph 5)

9. List of Acronyms and Initialisms

AC

Alternating Current

ACR

Adverse Condition Report

ALARA

As Low As Reasonably Achievable

ANF

Advanced Nuclear Fuels

ANSI

American National Standards Institute

APDMS

Axial Power Distribution Monitoring System

ASME

American Society of Mechanical Engineers

AVG

Average

BIT

Boron Injection Tank

C

Centigrade

CC

Component Cooling

25

CCW

Component Cooling Water

CFR

Code of Federal Regulations

CP&L

Carolina Power & Light

cpm

Counts Per Minute

CV

Containment Vessel

CWD

Control Wire Diagram

DC

Direct Current

DCN

Design Change Notice

EA

Enforcement Action

E & RC

Environmental and Radiation Control

e.g.

For Example

E-H

Electo-hydraulic

EAL

Emergency Action Level

EDG

Emergency Diesel Generator

EE

Engineering Evalution

EHC

Electro-Hydraulic Control

EQDP

Environmental Qualification Documentation Package

ERFIS

Emergency Response Facility Information System

EST

Engineering Surveillance Test

F

Fahrenheit

HCV

Hand Control Valve

gpm

Gallons Per Minute

HE & EC

Harris Energy and Environmental Center

HP

Health Physics

HVH

Heating Ventilation Handling

Hx

Heat Exchanger

I&C

Instrumentation & Control

IFI

Inspector Followup Item

IR

Inspection Report

JCO

Justification For Continued Operation

LCO

Limiting Condition for Operation

LER

Licensee Event Report

LOCA

Loss Of Coolant Accident

LP

Loop Calibration Procedure

M

Modification

MCC

Motor Control Center

MCP

Motor Circuit Protector

MIC

Microbiologically Induced Corrosion

MSIV

Main Steam Isolation Valve

NCR

Non-Conformance Report

NCV

Non-cited Violation

NFS

Nuclear Fuels Section

NI

Nuclear Instrumentation

NOV

Notice of Violation

NRC

Nuclear Regulatory Commission

OMM

Operations Management Manual

OP

Operations Procedure

PC

Protective Clothing

26

PIC

Process Instrument Calibration

PLP

Plant Program

PM

Preventive Maintenance

PNSC

Plant Nuclear Safety Committee

PPS

Penetration Pressurization System

Psig

Pounds Per Square Inch -

Gage

PSTG

Plant Specific Technical Guideline

PZR

Pressurizer

QC

Quality Control

RCCA

Rod Control Cluster Assembly

RCS

Reactor Coolant System

RHR

Residual Heat Removal

RO

Refueling Outage

RPI

Rod Position Indication

RTD

Resistence Temperature Detector

RTGB

Reactor Turbine Generator Board

RWP

Radiation Work Permit

SCR

Significant Condition Report

SFP

Spent Fuel Pool

SI

Safety Injection

SP

Special Procedure

SPP

Special Process Pocedure

SRO

Senior Reactor Operator

SW

Service Water

SWBP

Service Water Booster Pumps

TAVG

Temperature Average

TS

Technical Specification

URI

Unresolved Item

UV

Undervoltage

V

Voltage

VAC

Volts Alternating Current

VDC

Volts Direct Current

VIO

Violation

WR/JO

Work Request/Job Order