ML13323B269

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Insp Rept 50-206/87-05 on 870601-12.Violations & Deviations Noted.Major Areas Inspected:Determination of Effectiveness of Preventive & Corrective Maint Practices Re Equipment Degradation,Including Procurement & QA Programs,
ML13323B269
Person / Time
Site: San Onofre Southern California Edison icon.png
Issue date: 07/15/1987
From: Burdoin J, Caldwell C, Brendan Collins, Datta A, Eng P, Fiorelli G, Mclaughlin P, Jim Melfi, Richards S, Russell J, Sorensen R
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V), Office of Nuclear Reactor Regulation, NRC OFFICE OF NUCLEAR REGULATORY RESEARCH (RES)
To:
Shared Package
ML13323B267 List:
References
50-206-87-05, 50-206-87-5, NUDOCS 8707310138
Download: ML13323B269 (37)


See also: IR 05000206/1987005

Text

U. S. NUCLEAR REGULATORY COMMISSION

REGION V

Report No.

50-206/87-05

Docket No.

50-206

License No.

DPR-13

Licensee:

Southern California Edison Company

P. 0. Box 800

2244 Walnut Grove Avenue

Rosemead, California 91770

Facility Name:

San Onofre Nuclear Generating Station, Unit 1

Inspection at:

San Clemente, California

Inspection con

te

Inspectors:

F. B rd in, Project Inspector

Dfte Signed

C. W. Caldwell, Project Inspector

Date Signed

-7/I

G.- Fiorelli, Resident Inspector

Date Signed

V

F. ef

eactor Inspector

Date Signed

{lP. W.

aughinZ,

Office of Nuclear

Reactor egulation

frvA. a

, Office of Nuclear Regulatory

DitI (hned

Resea h

6e'P.

Ehg,

ident Inspector

Da

B. C

_

C o nsuZ

adSg

Rus elT, Radiatiab Specialist

Date Signed

R. C.

sen, Team Leader

Dat

8707310138 870717

PDR

ADOCK 0500206

DPeMige

-2

Approved By:

87&

-_

S. A. Richards, Chief

Date Signed

Engineering Section

Inspection Summary:

Inspection on June 1 -

June 12, 1987 (Report No. 50-206/87-05)

Areas Inspected:

Announced team inspection of San Onofre Nuclear Generating

Station (SONGS) Unit 1. The inspection focused on determining the

effectiveness of preventive and corrective maintenance practices in

preventing, or detecting and correcting, equipment degradation. The

inspection was conducted for a two week period during a 42-day mid-cycle

maintenance outage in Unit 1.

The following activities were examined:

1)

Procurement Program

2)

Quality Assurance Program

3) Operations

4)

Surveillance Testing

5)

I&C, Electrical and Mechanical Maintenance Practices

6) IST Program and Implementation

7)

Engineering

8)

Health Physics

This inspection was conducted by six NRC Region V inspectors, one NRC staff

engineer from NRR, one NRC staff engineer from the Office of Research, one NRC

inspector from Region III, and one contractor. Inspection Procedures 30702,

30703, 41400, 37700, 38701, 62700, 62704, 62705, 73756, 72701, 83729, 92701

and 92702 were applied to this inspection effort.

Results: Of the areas inspected, two violations of NRC requirements were

identified. One violation was identified in the area of providing adequate

information to permit individuals to take precautions to avoid or minimize

their exposure to radiation (paragraph 11) and one violation (two examples) was

identified in the area of demonstrating 125 volt vital battery no. 1 operable

(paragraph 2).

DETAILS

1.

Persons Contacted

San Onofre Nuclear Generating Station (SONGS)

  • H. B..Ray, Vice President and Site Manager
  • W*

C. Moody, Deputy Site Manager

  • H. E. Morgan, Station Manager

.*D. Heinicke, Deputy Station Manager

D. B. Schone, QA Manager

  • R. W.- Krieger, Operations Manager
  • D. E. Shull, Maintenance Manager
  • P. Knapp, Health Physics Manager

W_ G. Zintl, Compliance Manager

.*J. T. Reilly, Station Technical Manager

  • M. A. Wharton, Assistant Technical Manager
  • K. E. O'Connor, E&C Field Manager
  • H. W. Newton, Material Support Manager
  • M. 'P.

Short, Nuclear Training Manager

  • ,J.

J . Wambold-, Project.Manager

  • W. M. Lazear, A Supervisor
  • B. Katz, Manager, Outage Management
  • D. C. Stonecipher, QC Manager
  • G. D. Bogosian, QA Supervisor
  • K.

L. Brooks, Health Physics Supervisor

J. M. Joy, Outage Management Supervisor

  • R. D Plappert, Compliance Supervisor

'*K...Johnson, NSSS Engineering.Supervisor

J. Schramm, Operations Superintendent

  • L. 0. Cash, Unit 1 Maintenance Manager
  • C. A. Couser, Compliance Engineer

W.Denotesthose persons attending the final exit meeting on June 12, 1987.

The inspectors talked with numerous other licensee employees during the

course of the inspection

r

2C

Review of

Station Class 1E Batteries

a.

Battery Surveillance Testing

When the team arrived onsite on June 1, 1987, it was learned that

one of the station Class E batteries had failed a surveillance test

a short time before the team's arrival.

Since the objective of the

team inspection was to evaluate how well the licensee detected and

corrected equipment degradation, it was decided that this would be

an appropriate event to review in light of the team's objective.

The inspectors therefore reviewed, with the licensee, the results of

the service test that.was performed May 29, 1987 on 125 volt vital

battery no. 2. The batteryihad failed its service test since it

2

reached its low voltage limit after approximately 20 minutes of the

90 minute test. The licensee determined that the wrong load profile

values were used to perform the test. These values were from a

calculation sheet that had an extraneous load profile, i.e. a dotted

line on a graph, in addition to the actual load profile. These

extraneous load profile values were the ones used in the service

test.. This extraneous dotted line represented discharge rates that

were approximately twice as great as those of the correct load

profile.. Thus the battery reached its low voltage limit in 20

minutes. The test was halted when the battery terminal voltage

reached its low limit, thereby saving the battery cells from

potential damage due to cell reversal.

The inspectors noted that the calculation was prepared by one

engineer, reviewed by an independent engineer and two supervisors,

and issued by E&C. The calculations underwent various reviews by

Station Technical personnel and were then incorporated into the

service test procedure. However, no one in E&C, Station Technical,

or the maintenance personnel who wrote the procedure, caught, or

questioned the extraneous dotted line with the incorrect values

during the review process. As a result of this review and the

discrepancies identified, the inspectors questioned the values that

were used in the performance.of the service test on 125 volt vital

battery no. 1.

The inspectors reviewed the documentation that the licensee provided

for battery no. 1. This battery was installed on May 18, 1984 to

replace an aging battery. E&C personnel performed a load profile

calculation for this battery so that an acceptance test could be

performed. This load profile calculation, DC-1604 Rev. 0, was

performed on April 23, 1984 and was used in the acceptance test that

was performed on the battery on July 23, 1984.

On April 14, 1986, Rev. 1 to calculation DC-1604 was issued to

analyze the effect of adding 125 volt vital inverter 4A to the load

profile for battery no. 1. Shortly thereafter, Proposed Facility

Change (PFC) 1-86-3400.13 Rev. 0, was issued to add inverter 4A to

the plant. The inspectors reviewed the PFC and the new load profile

calculation along with licensee personnel. This PFC indicated that

the change to the plant had no impact on surveillances, Technical

Specifications, or limiting conditions for operation, as part of the

engineering/safety evaluation. However, that was incorrect, since

it did increase the load profile on battery no. 1 which affected the

service test surveillance procedure. Consequently, the need for a

change in the service test to include the load addition was not

identified and this load addition to the battery and the resulting

change in load profile were not included in the service test

procedure. As a result, on May 7, 1986, the battery no. 1 service

test was completed using the original Rev. 0 load profile

calculation. These values were less than the Rev. 1 values.

Therefore, the battery was not demonstrated operable in accordance

with station Technical Specification 4.4.0.2.d. This is a violation

of Technical Specification requirements (87-05-01). The inspectors

noted that in this case also,, the PFC was reviewed and approved by

3

various independent and supervisory E&C and Station Technical

personnel.

However, nobody recognized that a change to the service,

test procedure was required.

As a further example of missed opportunities, the inspectors noted

that on May 7, 1986, the Independent Safety Engineering Group (ISEG)

issued a report on an evaluation they did of the PFC administrative

procedure. ISEG recommended in their report that the PFC procedure

be revised to require that a new load calculation be performed

whenever it is determined that a load is added to the batteries.

Upon receipt of the new calculation, Station Technical should assess

the need for modification of the battery surveillance procedures and

provide the information to Maintenance as necessary. During the

turnover of vital inverter 4A, it was discovered that an Appendix R

and a seismic qualification evaluation were needed for this

component. Therefore, it was not placed in service until a few

months later. On July 15, 1986, Rev. 1 to PFC 1-86-3400.13 that

added inverter 4A was issued. This revised PFC also indicated that

the calculation had been updated but incorrectly stated that there

was no impact on existing surveillance requirements, Technical

Specifications, or limiting conditions for operations in the

engineering/safety evaluation. Therefore, the service test

procedures were not revised to include the new load.profile. Again,

the PFC underwent various levels of review by E&C and Station

Technical personnel.. The May 7, 1986 ISEG report recommendation

discussed previously, was incorporated as temporary change (TCN) 6-1

to the PFC procedure. The ISEG report was issued 2 months prior to

PFC 1-86-3400.13 Rev. 1 but TCN 6-1 was not added to the PFC

procedure until 6 months later on November 13, 1986. If this change

had been made prior to issue of the revised PFC, it would have

required that an assessment be made of the new calculation for the

need to modify the surveillance procedures and provide the

information to Maintenance as necessary. This could have prevented

the use of the wrong calculation in the service test procedure.

Over the next few months several other changes were made to the

battery no..1 load profile. On September 15, 1986, Rev 2 to

calculation DC-1604 was issued which reflected increases to the

battery no. 1 load as part of a "worst case adjusted load" profile.

On February 12, 1987, PFC 1-87-3465 Rev. 0 was issued to remove the

regulating transformer for inverter 4A. This caused a slight load

reduction on battery no. 1.

On May 22, 1987, the scheduled refueling interval service test was

performed. Again, the load profile values from calculation DC-1604

Rev. 0 were used. These values were still less than the Rev. 2

values. Therefore, the battery was not demonstrated operable for a

second time in accordance with station Technical Specification 4.4.0.2.d. This is a further example of violation (87-05-01).

Ih addition, an extraneous 815 amp discharge rate was included

somehow on page 9 of the DC-1604, Rev. 2 calculation. This value is

labeled as representing the original load duty cycle andas being

superceded by section 7.2 of the calculation. Section 7.2 shows the

4

value as 800 amps. Procedural reviews did not catch or question

this error.

Based on these discrepancies, the inspectors questioned the load

values used in the acceptance test performed on battery no. 1 in

1984. The acceptance test consisted of a service test and a

performance test. The inspectors noted that the service test

portion was performed satisfactorily. However, the inspectors were

concerned about the values used in the performance test portion.

That portion required that the battery be discharged at a value

specified by the vendor for a certain period of time. In this case,

the time period was 90 minutes. The procedure indicated that the

battery be discharged for this period at 1240 amps.

Licensee

personnel evaluated the calculations upon the inspectors' request

and determined that the value that should have been used was 944

amps. Once again, the values that were provided by E&C were

incorrect and were incorporated into station procedures. In this

case however, the test was performed in a conservative manner,

although this still indicates a laxness in the performance of

technical work.

As a result of these problems the licensee took aggressive action

toward resolving the deficiencies identified in past battery service

tests. The license issued several non-conformance reports (NCRs) to

identify the battery service test problems and to propose corrective

action. In addition, the QA organization prepared two CARs that

will be used to perform a generic evaluation of the design control

process. The licensee committed to correct the deficiencies in

accordance with an interim root cause analysis, Rev. 1, dated June

9, 1987, as follows:

1.

Prepare a TCN to battery surveillance procedure S01-I-2.7 to

test per the calculation DC-1399, Rev. 2, documented load

profile for battery no. 2.

2. Add a step to record battery voltage at the end of the 90th

minute, prior to removing the load current, for future

reference.

3.

Require that the Individual Cell Voltages (ICVs) be recorded

during the load test so that any failed cell can be identified

after the first load test. (This should have been done

previously as a good engineering practice).

4.

Revise station maintenance procedures for all 3 units' battery

service tests to:

0

require that the station cognizant engineer document the

revision of the calculation in effect during the last

battery service test, document the current revision of the

applicable battery load calculation and verify that the

load profile within the maintenance procedure correctly

applies to the calculated load profile.

5

Clearly specify the required wait time after an equalizing

charge prior to starting a service or performance test.

5.

Review E&C QA procedures for "Proposed Facility Changes" and

revise as required to ensure that modifications that alter the

battery loading require re-analysis of the battery load

calculations and reperfomance of the battery service test as

necessary. This was completed per TCN 6-1 to the PFC

procedure.

6. A refueling interval battery service test will be performed on

battery no. 1 in accordance with Calculation DC-1604, Rev. 2,

and PFC 1-87-3465 prior to Mode 4 entry.

7. Expand the review of battery calculations and refueling

interval service test procedures to include the remaining Unit

1 batteries and all Units 2 and 3 batteries.

8.

Review and revise, as required, the battery maintenance

procedures and operating instructions for Units 1, 2, and 3 for

uniformity and adequacy and to add specific definitions of

battery operability requirements following maintenance.

9.

Perform further analysis, by the QA organization, of the

problems identified with the design review process.

CARs

SO-P-1049 and SO-P-1050 have been issued in order to evaluate

why testing was performed on the batteries with the incorrect

acceptance criteria provided in the procedure and why the

configuration document checklist did not show that there needed

to be a change to the discharge procedure.

As a followup to the discrepancies identified, the licensee

performed service tests of both battery no. 1 and 2 prior to startup

of the unit. Both batteries passed these tests and were

demonstrated operable.

b.

System Physical Walkdown

The inspector conducted observations of equipment and component

rooms to determine if they were being maintained in accordance with

station procedures and regulatory requirments.

In general, components, systems, and areas appeared to be well

maintained and in good physical condition. However, the inspector

identified the following concerns to the licensee for evaluation:

Battery no. 1 battery has styrofoam end spacers located at one

end of each row of battery jars. This could potentially

jeopardize the seismic qualification of the battery. This

concern was identified to the licensee for evaluation. The

inspector will review the licensee's evaluation. This is

identified as inspector followup item (87-05-02).

6

There were two bottles used as portable eyewash stations

located in battery no. 2 room. One of the eyewash stations was

secured to safety related conduit that contained the battery

cables. This was done by using a long chain. This bottle, as

installed, could damage several battery jars or damage the

battery connectors if a seismic event should occur. Station

procedure S0123-1-1.20 Rev 1, denotes the controls that are in

place to ensure that every reasonable effort is made to prevent

impairment of any safety related system

Section 6.1.1

requires that precautions shall be taken to ensure that no

tool, material, or any other item capable of damaging a

safety-related piece of equipment be allowed to impact any

safety-related equipment. The inspector was concerned that

even though there is a procedure in place to protect

safety-related equipment, personnel are not adhering strictly

to the procedure. Similar conditions have been previously

identified in resident inspection report 50-206/87-03. The

licensee's corrective actions on controls over items located

near safety-related equipment will be followed in a future

resident inspector report.

3. Modification Testing

To evaluate the licensee's program for modification testing, several of

the licensee's documents which describe their program for testing were

reviewed. These documents include administrative procedures for testing

and are listed below:

Topical Quality Assurance Manual, Chapter 6-C Construction

Inspection and Testing.

Topical Quality Assurance Manual, Chapter 6-0 Prerequisite,

Preoperational, and Startup Testing.

Retrofit Program Manual, Volume II, Administrative Procedure AP-4

(S0123-AP-004) Preparation, Review and Approval of Prerequisite Test

Procedures.

Retrofit Program Manual, Volume II, Administrative Procedure AP-5

(S0123-AP-005) Preparation, Review and Approval of Preoperational

Testing Procedures.

Retrofit Program Manual, Volume II, Administrative Procedure AP-6

(S0123-XXVI-2.6) Review, Evaluation and Approval of Test Results.

-

Retrofit Program Manual, Volume II, Administrative Procedure AP-7

Test Working Group.

The test procedures that were used during the modification activities

which were reviewed were:

Instrument and Test Procedure, 501-I1-1.32, Pneumatic Valve

0

Cal ibrati on.

7

Instrument and Test Procedure, S0123-I1-9.37, Control Valve

Calibration.

Generic Test Procedure, GT-400-14 (S0123-XXVI-6.4.14), Circuit and

Calibration Tests.

Because of the dates of the inspection, most of the modifications planned

for this-outage were completed prior to the team's arrival.

Most of the

Construction Work Orders (CWOs) which were reviewed had already been

performed, signed-off, and sent to configuration control for final

documentation. Therefore, there were very few opportunities for

observing actual modification testing being performed.

The following CWOs were reviewed during this inspection:

87031251000, S1-RSS-CV-948-ACT, PRT Gas Space Sample Actuator (Valve

Preload Setting)

87060463000, S1-ELE-Y14, 120V Vital Bus 4 (Transfer Switch

Modification)

87030385000, S1-DG1-EO8, L.V. Exciter Cabinet DGI (Conduit and

Cable)

- 86051181000, S1-VCC-2159, Discharge Solenoid Valve from Charging

Pumps Suction Header (Piping)

87020467000, S1-MVS-MSH-4109, A-33 Fan Intake High Humidity Switch

(Switch Installation)

- 87030912000, S1-MVS-A-33, Emergency Makeup Fan for A-31 (Power On

Mechanical Testing)

Two of the CWs were examined in more detail than the others. For an

example of a CWO which had been completed, CWO # 87031251000 was used.

The CWO selected for in-field inspection was CWO # 87060463000.

During the review of the completed CWO (87031251000), it was found that

the test procedure identified to be used in the work package had been

superseded by another procedure. Based on the dates on the CWO for

planning and approval of the work order, the superseding had occurred

prior to the development of the CWO.

However, the technician identified

the proper test procedure when he began working on the task. The

inspector felt that the incorrect test procedure should have been

identified during the approval process. Upon questioning QA personnel,

they stated that the approval dates on the procedure don't always reflect

when the procedure was developed (the procedure is often prepared long

before those dates that appear). They also stated that this is an

example of why the CWOs always include a step for the technician to

assure he has the most recent revision of the procedure.

As a result of'these conversations with QA, several QA Field Surveillance

Reports were reviewed. These reports indicated that minor discrepancies

I

8

similar to the one noted above occur and are resolved by the technicians

per program guidelines.

While observing work in the Unit 1 Control Room, a problem arose

concerning the functional testing required by CWO 87060463000. This CWO,

which affected Vital Bus #4, referenced a generic test procedure for

performing the functional test on a design modification. When the

reactor operator requested clarification as to what the functional test

affected, the technicians and cognizant engineer generated a two (2) page

"back of the envelope" type procedure. After the operator expressed

concern about performing parts of the test, the shift superintendent

interjected and said the work would not be done until the informal

procedure was evaluated and approved by engineering personnel. The CWO

was subsequently revised to include these steps and plans were made to

perform the test.

Startup Engineering's position is that this "back of the envelope"

process is a type of "tailboarding" and takes place all the time. Also,

the Generic Test Procedure for Circuit and Calibration Tests is often

approved and used for modification testing. However, the fact that the

reactor operator requested more information and the shift superintendent

requested engineering approval reflects the inadequacies of using generic

test procedures for performing tests. The inspector contends that the

generic test procedure should only be used to develop a detailed

procedure (similar to the one subsequently generated by Startup

Engineering).

Further, at the QC holdpoint in the CWO, it was not clear

what the QC inspector was specifically required to verify.

Although no violations or deviations were identified, several concerns

were identified regarding this program.

The previous example illustrates a lack of engineering effort in the area

of test procedure preparation and planning for post modification testing.

The test procedure was inadequate and appeared to have no engineering

guidance or management approval.

The "back of the envelope" approach is

not suitable for the testing of safety-related equipment. This less than

rigorous effort by Startup Engineering is another example of a weakness

in the performance of technical work.

4.

Inservice Testing Program

a. Overall Program Status

San Onofre Nuclear Generating Station, Unit 1, is currently in their

first ten year inspection interval which is scheduled to end on

December 31, 1987. The licensee is currently in the process of

updating their Inservice Testing (IST) program in preparation for

the second ten year program. Current valve and pump test programs

are written to comply with the requirements of the 1977 Edition of

the American Society of Mechanical Engineers' Boiler and Pressure

Vessel Code, up to and including the Winter 1979 Addendum.

By letter dated December 22, 1977, the Division of Operating

Reactors advised the licensee to implement the proposed IST program

.

9

until a detailed review of the program was completed. As of the

date of this inspection, the licensee's IST program had not been

approved.

b.

Inservice Testing of Valves Program

The licensee delineates the policies and procedures for inservice

testing of valves in the following procedures:

S0123-IN-1, In-Service Inspection Program

S01-V-2.15, In-Service Testing of Valves Program

S01-12.4-2, Operations In-Service Valve Testing

S0123-V-5.15, Inservice Testing (IST) Coordination and Trending

The inspector reviewed the valve inservice testing requirements.

Based on this review which included the NRC findings related to the

November 21, 1985 loss of power and water hammer event at San Onofre

Unit 1, documented in NUREG-1190, the inspector determined that the

valve inservice program was based on the ASME Boiler and Pressure

Vessel Code,Section XI,.which specifies valve inservice testing

(IST) requirements, and states in part:

Valves shall be exercised to the position required to fulfill

their function unless such operation is not practical during

plant operation....

Valves that cannot be exercised during

plant operation shall be specifically identified by the owner

and shall be full-stroke exercised during cold shutdowns.

Full-stroke exercising during cold shutdowns for all valves not

full-stroke exercised during plant operation shall be on a

frequency determined by the intervals between shutdowns as

follows:

for intervals of 3 months or longer, exercise during

each shutdown; for intervals of less than 3 months, full-stroke

exercise is not required unless 3 months have passed since last

shutdown exercise.

Further review of the licensee's program revealed that Step

6.3.1.2.d of licensee procedure SO1-V-2.15 states that "As a matter

of policy, an initial requirement of 25% (minimum) of all cold

shutdown valves will be tested each Mode 5 forced outage."

Item K

of Attachment 1 to the same procedure states, "Valve testing at cold

shutdown is valve testing which commences not later than forty-eight

hours after cold shutdown and continues until required testing is

completed or Plant startup, whichever occurs first....

Completion

of all required valve testing is not a requisite to Plant startup.

Valve testing which is not completed during a cold shutdown will be

performed during subsequent cold shutdowns...."

The inspector noted that during the only Mode 5 shutdown since the

water hammer event that occurred September 4-28, 1986 (excluding the

current mid cycle outage) 40% of the valves listed on the cold

10

shutdown test list were tested. During the current outage all of

the valves listed on the cold shutdpwn test list will be tested.

The inspector inquired as to the changes made to the valve IST

program resulting from the water hammer event of November 21, 1985.

The licensee stated that 17 check valves in the feedwater system and

the auxiliary feedwater system had been replaced after the event and

that these check valves are full stroked and leak tested at every

cold shutdown. Review of the valve program revealed that although

the valve test requirements had been revised, the valves in question

were still designated as category "C".

The licensee agreed to

revise the valve categories for the 17 check valves in their next

IST program submittal to NRR. Revision of the licensee's valve IST

program to reflect the valve recategorization of the 17 check valves

will be tracked as an open item (87-05-03).

The inspector inquired whether valves which can be controlled from

the licensee's dedicated shutdown (DSD) panel were included in the

valve IST program. The licensee stated that there was only one

valve whose position was indicated on the DSD panel and that the

valve in question, FCV-5051, was not included in the IST program.

IWV-1100 defines the scope of IST testing for valves to encompass

"those valves which are required to perform a specific function in

shutting down a reactor... or in mitigating the consequences of an

accident."

IWV-3300 states that valves with remote position

indicators shall be observed at least once every 2 years to verify

that valve operation is accurately indicated. Although the DSD

panel has been in place for approximately a year, the inspector

noted that FCV-5051 had not been included in the valve IST program

as submitted to the Commission. The licensee's QA organization

initiated a Problem Review Report (PRR) to address this concern.

The inspector will follow the licensee's resolution of this concern

(50-206/87-05-04).

No violations or deviations were identified.

c. Valve Testing

The inspector reviewed selected valve test procedures and noted that

the method to be used for obtaining valve stroke times was not

specified. The licensee stated that a valve stroke time technique

would be added to the appropriate procedures to ensure valve stroke

timing consistency in accordance with the requirements of

IWV-3413(a), by August 1, 1987. Incorporation of a specific valve

stroke timing method to valve test procedures by the licensee will

be tracked as an open item (87-05-05).

Subsection IWV-2300 of Section XI defines valve exercising as "the

demonstration based on direct or indirect visual or other positive

indication that moving parts of a valve function satisfactorily."

IWV-3413 provides for the limiting value of full stroke time as one

of the criteria for test acceptance. Consequently, stroke time

limits for valves must be chosen such that operation within such

limits indicate satisfactory valve condition. Several of the

11

maximum allowable stroke times, as defined by the licensee, are not

adequate for this purpose. For example, several valves that

typically stroke in less than 10 seconds are assigned maximum valve

stroke time values of up to 120 seconds. The inspector noted that

the maximum allowable stroke times have been submitted to'NRR for

review.

The licensee stated that, although they assign maximum stroke times

of up to 120 seconds, they initiate corrective action on valves

based on the criteria delineated in IWV-3417, which is triggered on

significant increases in stroke time from the-last valve stroke time

test.

d.

Inservice Testing of Pumps Program

The licensee delineates the policies and procedures for inservice

testing of pumps in the following procedures:

S0123-IN-1, In-Service Inspection Program

SO1-V-2.14, In-Service Testing of Pumps Program

S0123-V-5.15, In-Service Testing (IST) Coordination and

Trending

The inspector reviewed licensee relief requests for the IST of pumps

and noted that a relief request addressing the expansion of the

allowed full scale range of inservice testing instruments from three

times the reference value to four times the reference value had been

submitted -to the Commission. IWP-4120 states that the full scale

range of each instrument shall be three times the reference value or

less. Since there appears to be no basis for the licensee's relief

request, the licensee's QA department agreed to pursue resolution of

this discrepancy.

The inspector noted that the licensee had not established acceptance

criteria for pump bearing temperatures based on the manufacturer's

recommendations. This item was also identified in a recent QA audit

of the licensee's IST program and will be resolved by June 30, 1987.

e.

Inservice Testing Performance

The inspector witnessed the inservice testing of the G-10W electric

driven auxiliary feedwater pump. The test engineer performed the

pertinent portions of test procedure SO1-V-2.14.1, "Auxiliary

Feedwater In-Service Pump Test" in accordance with the requirements

of the procedure. Prior to and during test performance both the

cognizant engineer and the equipment operator repeatedly inspected

the material condition of the pump and associated piping and valves.

Test.data was obtained in general agreement with the methodology

specified in the Code; however, the inspector noted that neither the

test procedure nor the physical pump installation had provided for

identifying the locations on the pump and motor bearing where

vibration data was to be obtained. IWP-4160 states that instruments

12

that are position sensitive shall be either permanently mounted or

provision shall be made to duplicate the position for each test.

IWP-4520 allows use of a portable vibration indicator that clearly

identifies the probe or measurement reference point to permit

subsequent duplication in both location and plane. The licensee

stated that vibration measurements on pumps in the IST program are

taken by the system cognizant engineer who knows where to take

vibration readings, and several system cognizant engineers stated

that they always measured vibration at the same point from test to

test. Review of pump test data by the inspector could not identify

instances where failure to measure bearing vibration at specific

points per the requirements of the Code was key in determining pump

operability. The inspector stated that should the cognizant

engineer be unavailable to perform IST tests in the future, the

locations for obtaining pump vibration data for IST purposes would

be subject to question. The licensee stated that an evaluation of

an appropriate method to clearly define points where IST vibration

data is to be taken would be performed and incorporated into the

pertinent IST test procedures for all 19 pumps in the IST program by

July 15, 1987. Completion of incorporation of vibration data point

locations into licensee procedures for all pumps in the IST program

will be tracked as an open item (87-05-06).

During performance of the Auxiliary Feedwater pump G-10W test, the

inspector noted that the lubricant in the slinger ring region

appeared to be the consistency of syrup. The cognizant engineer

stated that he would request that the oil be sampled and changed.

The inspector also noticed a lube oil addition log sheet stored on

the side.of the pump motor housing which is subjected to the

prevailing.environment and was becoming hard to read. The cognizant

engineer stated that the copy observed by the inspector was a field

copy and not the official records copy.

f. Quality Assurance Audits of IST Programs

The inspector reviewed the licensee's latest QA audit (SCES-042-86)

of the implementation of the IST program and noted that the audit

was both comprehensive and thorough. Identified findings were

pertinent, appropriate, and similar to violations identified during

typical Commission inspections of IST program implementation at

other facilities. The inspector noted that the items identified

were in the process of being corrected by the technical staff. The

inspector also noted that several comments were made in the audit

text which were not specifically identified as deficiencies in the

audit report, the most notable of which was the lack of

identification of those locations on Unit 1 pump installations where

vibration data for IST testing was to be obtained (see paragraph e).

The inspector also noted that the QA audit recognized that vibration

measurement locations for pumps in the Units 2 and 3 IST program

were identified in the Units 2 and 3 test procedures.

Within the areas inspected, no violations or deviations were identified.

13

5.

Procurement

The inspector reviewed the licensee s program for procurement. This

included a review of procedures, purchase orders, and other documentation

used in the procurement process to determine if the program was being

properly implemented.

The following SONGS' procedures governing the material procurement

process were reviewed.

Material Control Procedure

S0123-XI-1.4

Upgrading an Item's Quality Class

-

Material Control Procedure

S0123-XI-2.0

Procurement Document Control

Material Control Procedure

50123-XI-2.1

The Five-Level Procurement System

Material Control Procedure

S0123-XI-2.3

Verification Test Procedures

Material Control Procedure

S0123-XI-2.5

Substitution Part Equivalency Evaluation Report (SPEER)

Material Control Procedure

S0123-XI-2.6

Critical Characteristics Evaluation

Quality Assurance Procedure

E&C37-26-16

Procurement of Items and Services for SONGS 1, 2, & 3,

Engineering and Construction Projects

In addition, over 200 samples of completed Purchase Orders, Spare Part

Equivalency Evaluation Reports (SPEERS), evaluations for placement of

items on the safety-related commodity list and Stock Upgrade Requirements

Evaluations (SURES) were reviewed. Staff representatives of the Material

Support Division and Station Technical Division were interviewed to

ascertain qualifications and responsibilities concerning their

procurement duties.

The SONGS' material procurement program was evaluated for compliance with

10 CFR 50, Appendix B, the procedures governing the program, and sound

engineering principles applicable to procurement of spare parts for

safety-related equipment.

During this inspection, the inspector identified one significant

programmatic weakness. The inspector noted a pervasive lack of rigor to

fully document engineering evaluations conducted to approve spare and

replacement part substitutions or upgrades. An example of this lack of

rigor is contained in SPEER 87-0071. In this example, the licensee

approved the substitution of a 3" globe valve on the master valve list

with a valve of significantly different configuration. This valve has

many applications in the plant. However, the licensee's documentation of

their evaluation failed to show any consideration of a seismic load

14

analysis performed on safety-related piping runs where the new valve

could be installed. The seismic load analysis could be significant since

the new valve assembly weighs approximately 10 pounds more than the valve

being replaced.

This laxness to fully and professionally document the technical bases

considered during these evaluations could result in possible significant

information being overlooked during any subsequent reviews concerning the

installation of substituted or upgraded parts in the plant. Also, since

SONGS engineering analysis responsibilities for part procurement,

substitution, and installation are split between Procurement Engineering,

Station Technical Engineering, and E&C, the full disclosure of all

information-pertinent to the analysis must be.provided for consideration

by each of these various engineering organizations. Better documentation

of the engineering analyses performed by each engineering organization

could preclude the possible installation of an unauthorized, improper

part in the plant.

Of the areas inspected, no violations or deviations were identified.

6. Quality Assurance

The inspection of this area included the review of the program documents

and procedures governing the conduct of the quality assurance activities

at SONGS. Interviews were held with QA engineers, QC inspectors,

auditors, and supervisors concerning their experience, training,

responsibilities, and activities on site. Six completed audit surveys

were reviewed. The resulting Corrective Action Requests (CARS) and their

subsequent disposition were also reviewed. In-field QC inspections of

ongoing maintenance work were observed. The QA/QC activities of SONGS

incoming inspection of receiving materials were reviewed and observed.

The licensee's performance in this area was evaluated against the

requirements of 10 CFR 50, Appendix B and the guidance contained in

ANSI/ANS 3.2. The completed audits and inspection documents were

reviewed to ascertain if the completed work had been performed in

accordance with the applicable SONGS procedures. The inspector noted

that the completed audits were thorough, professional and in-depth. This

was considered a strength of the QA program. It was also noted that the

average time required to close a Corrective Action Request (CAR) was 66

days. This was based on a 1-year sample of 102 closed CARS. This was

considered to be a satisfactory resolution time for CARs.

No violations or deviations were identified.

7.

Reactor Operations

The inspector reviewed reactor operations related activities associated

with the current midcycle maintenance outage. The plant was in Mode 5

during the inspection period and the following types of activities and

plant configurations were reviewed and observed.

-

System alignments.

15

.Conformance with Technical Specification Limiting Conditions for

Operation for Mode 5.

- Chemical analyses of primary coolant, refueling water storage tank

contents, and diesel generator fuel oil.

Control room and shift superintendent log entries.

Plant housekeeping.

Implementation of temporary modifications.

Implementation of clearance-and tagging controls.

The inspector observed that formal approved procedures existed for the

control of the observed activities. Records contained required

documentation confirming executed activities and configuration control.

Plant staffing was consistent with Technical Specification requirements

and discussions with plant personnel revealed the staff to be

knowledgeable of plant design and operation. The plant was in midloop

operation for the greater portion of the inspection period. Control room

instrumentation was observed to provide the required vessel level

information. Adequate shutdown margin was observed to have been met. An

inspection of control room panel areas revealed housekeeping to be

adequate. No unauthorized jumpers were observed.

While touring one of the emergency diesel generator rooms, the inspector

noted a storage room that contained bottles of fuel oil samples, oily

rags, and spilled fuel oil on shelves. Operations personnel have

exclusive use of this storage room, and it appeared to be used mainly for

diesel fuel oil sample storage.

Discussions with licensee fire protection personnel indicated that the

combustible loading for the diesel generator room in question, of which

the storage room was considered a part, was much greater than that

represented by the materials in the storage room. Therefore, they were

not considered a fire hazard from an Appendix R point of view, since the

licensee has installed a.dedicated shutdown diesel, for Appendix R

purposes, in a different area of the plant. However, the inspector was

still concerned that the combustibles located in the storage room

presented an undue fire hazard to safety related equipment. During a

subsequent tour of the area with the Operations Manager, the inspector

observed that it had been cleaned up noticeably. The Operations Manager

stated he would develop a policy statement to instruct operations

personnel on the storage of combustible material in this room.

No violations or deviations were identified.

8.

Surveillance Testing

The inspector reviewed the licensee's surveillance program for compliance

with established requirements. This review covered the following areas:

16

Observations associated with the local leak rate testing of 3

penetration volumes, Nos. 27, 28 and 32.

Observations associated with the conduct of the Safety

Injection/Loss of Offsite Power test.

The review of twenty completed surveillance tests.

The inspector noted that surveillance tests required by Technical

Specifications had been identified and listed in a controlling document.

The completed tests reviewed were performed using formal approved

procedures. Required test data was documented, prerequisites were

completed, acceptance criteria were met, and test results were approved

by operations supervision. The tests reviewed by the inspector were

completed at the required frequencies.

The inspector noted, during the performance of surveillance test

501-12.8.2, "Cold SIS and Loss of Offsite Power Test," that a thorough

pretest briefing had been held with the staff involved in performing the

test. Communications and direction given during the test were effective

and clear, and the control room personnel were serious and attentive. A

formal approved procedure was written for the test and was checked as

being the most current revision.

The local leak rate testing was performed in accordance with approved

procedure SO1-V-1.12 "Containment Penetration Leak Rate Testing."

Pretest meetings were held with control room operations staff and health

physics personnel.

The inspector observed that a test pressure slightly

in excess of 50 psig was applied to the penetration volumes in accordance

with test procedures. Valving configurations were checked out in

accordance with procedures and test data was properly documented.

Pressure gauges and stop watches had current calibration dates. Test

engineers were knowledgeable of plant design and testing requirements.

In the case of penetration volume 32, a retest was required as one of the

boundary valves would not hold pressure.

One violation was identified in the area of surveillance testing, which

dealt with station vital batteries, and is discussed in detail in

paragraph 2.

9. Observation of Maintenance Activities

The licensee's maintenance program was examined to evaluate the

effectiveness of the program and to determine whether or not corrective

and preventive maintenance were being conducted in accordance with

regulatory requirements and licensee-approved procedures and

instructions. Maintenance for Unit 1 was inspected in four areas:

electrical, instrumentation and control, pumps, and mechanical.

a. Electrical

The electrical maintenance program was inspected by examining the

following procedures that describe the functioning and the

administration of the program:

-

17

Quality Assurance Program Chapter 5-C, "Maintenance Program"

Maintenance Procedure 50123-1-1.6, "Maintenance Section Policy

Guidelines"

Maintenance Procedure S0123-I-1.7, "Maintenance Order

Preparation, Use and Scheduling"

These procedures detail the administrative controls necessary to

identify, plan and schedule routine and nonroutine maintenance.

Instructions for initiating and preparing a maintenance order (MO),

the principal device for accomplishing maintenance work, is

contained in procedure S0123-I-1.7.

The inspector examined the following electrical MOs completed during

this shutdown period to verify that the program for performing

electrical maintenance was being conducted in accordance with

established procedures. These MOs were examined for content, proper

authorization signatures, QC participation, job completion sign-off,

QA review, etc.

86031447000, Perform Disposition of NCR S01-P-5899, Implement

FCN's SI-767E and SI-768E and Perform Movats Test per IEB

85-03.

86052779002, Safety Injection Pump Discharge Check Valve

Miscellaneous Maintenance.

87051345000, Replace Unqualified Butt Splices per Disposition

on NCR SO1-P-6114.

8705148000, Remove Motor Mounting Bolts to Allow for Coupling

Removal on Safety Injection Pump Motor West.

87051479000, Remove Motor Mounting Bolts to Allow for Coupling

Removal on Safety Injection Pump Motor East.

87041416001, HV851A Replace Limit Switch with E/Q Namco EA 180

Limit Switch and Replace Conduit Seal.

87041411001, HV-853A Replace Limit Switch with E/Q Namco EA 180

Limit Switch and Replace Conduit Seals.

-

87041415001, HV-852A Replace Limit Switch with E/Q Namco EA 180

Limit Switch and Replace Conduit Seals.

-

87010075001, Permanently Attach SV-1 Terminal Block to the back

of the J Box per NCR S01-P-6034.

-

87060355001, Feedwater Block Valve Actuator, Repair Motor and

Replace Lugs. Inspect Limit Switch Wiring per Applicable

Drawings.

18

87033305000, Inspect Terminal Blocks, and Check Locknuts

Bushings for Tightness in-all Hoffman J. Boxes on HV-851 A/B,

852 A/B, 853 A/B and 854 A/B.

The above MOs appeared to be in order and appeared to have been

processed in accordance with prescribed procedures.

A field inspection was made of work in progress in the plant

involving main feedwater pumps. The replacement of limit switches

with EQ Namco EA 180 switches on valves HV-853B and HV-854B under

MOs 87041414001 and 87041421001 respectively was taking place. The

work appeared to be progressing in accordance with the description

and instructions in the MOs.

The inspector examined audit SCES-007-86 dated June 23, 1986

performed by quality assurance to verify that documentation,

instructions and controls have been established and implemented in

accordance with topical quality assurance manual, chapters 5-C and

7-D for the station maintenance program. The audit team was made up

of four members and was conducted during a six week period in 1986.

The audit assessment of.root causes of significant deficiencies was

"no significant deficiencies have been identified".

The inspector examined in detail the audit plan items (eight) and

findings for each of these items which were included in the audit

report. The audit, the plan and the findings and conclusions

appeared to be in order..

The inspector concluded that the electrical maintenance appeared to

be accomplished in accordance with the program as described in the

applicable procedures and appeared to be adequate.

b.

Instrumentation Maintenance

The examination of the Instrumentation and Control (I&C) Systems

Maintenance Program at SONGS-1 included a review of the licensee's

program as described in the following licensee documents:

Topical Quality Assurance Manual, Chapter 5-C Maintenance

Program

Maintenance Procedure, 50123-1-1.3, Maintenance Documentation.

-

Maintenance Procedure, S0123-I-1.6, Maintenance Section Policy

Guidelines.

-

Maintenance Procedure, S0123-I-1.7, Maintenance Order

Preparation, Use,. and Scheduling.

After evaluating the overall maintenance program, specific test

procedures were reviewed. Some of the procedures applied to Unit 1

only (SO-), and other procedures were for all of the San Onofre

units (S0123-). The specific I&C procedures that were examined in

detail were:

19

Instrument and Test Procedure, S01-II-1.2, Surveillance

Requirement Reactor Plant Instrumentation Test.

Instrument and Test Procedure, S01-II-1.20, Nuclear

Instrumentation System Detector Replacement.

Instrument and Test Procedure, SO1-II-1.72, Intermediate Range

Compensating Voltage Adjustment.

Instrument and Test Procedure, SO1-II-1.76, Surveillance

Requirement Auxiliary Feedwater System Test.

Instrument and Test Procedure, SO123-II-8.10.1, Electronic Loop

Verification.

Instrument and Test Procedure, S0123-II-9.37, Control Valve

Calibration.

Instrument and Test Procedure, S0123-II-9.82, Pressure Switch

Calibration.

Several MOs were reviewed for conformance to the station

requirements as described in the maintenance program and procedures.

The MOs were-reviewed for the use of correct and current procedures,

adequate instructions and QC "HOLD" points, identification of

prerequisites, description of test requirements, and listings of

required test equipment. The MOs were evaluated at different stages

of the maintenance process. --

Some of the MOs were in planning,. some

were being worked in the field, and some had been completed and

signed off.

The MOs which were in the planning stage were briefly reviewed for

adherence to the program guidelines.

Several of the jobs being performed in the field were evaluated by

observing the I&C personnel performing their assigned tasks. The

work orders were examined to ensure that the technicians were

following the instructions presented in the MOs and properly

documenting the work being performed.

For MOs in which the work had been completed, the documentation was

examined for completeness, to verify that the procedures had been

followed, and that the "HOLD" points had been observed. Special

attention was given to the presence of signatures and comments

concerning the work performed.

The MOs examined in one of these three stages during this inspection

were:

86042580000,S1-72-130, B Train Hi.gh Voltage Control Power

(Agastat Relay Replacement)

-.

86091581000,S1-DEN-1GA2C15-187, DG2 Generator Differential

Relay (Modification to SA-1 Relay)

20

86110753000, S1-RCS-G-2B, 'B' Reactor Coolant Pump

(Instrumentation Removal/Reinstallation)

86111907000, S1-AFW-PT-2010, NPSH XMTR-G-10S (Calibrate

Pressure Transmitters)

86111909000, S1-CVS-PT-1120A, Containment Hi Pressure Train A

(Containment Isolation System Calibration)

87030632000, S1-AFW-PYV-3010, Current to Voltage Converter

(Auxiliary Feedwater System Calibration (Train B))

87031063000, S1-FWS-FCV-457, Main Feedwater Flow Control-SG/B

(Valve Response Data Collection)

-

87032621000, S1-NIS-N-1207, Power Range Channel 1207 (Detector

Replacement)

-

87050552000, S1-AFW-FTL-3453, Differential Pressure Low Flow

Transmitter (Auxiliary Feedwater Full Flow Test)

87051611000, S1-NIS-N-1203, Intermediate Range Channel 1203

Channel Checkout)

As a result of this inspection, implementation of the SONGS-1 I&C

Maintenance Program-was found to be consistent with procedural

requirements.

The personnel responsible for the I&C maintenance had

a good knowledge of the program and systematically tracked and

performed the required tasks.

c.

Pumps

The inspector examined work control documentation, interviewed

licensee personnel involved in pump maintenance and testing, and

examined work in progress on various safety-related and non-safety

related pumps.. The objective was to determine whether modifications

being made to these pumps,.because of problems identified by the

licensee, were reasonable and sound from a technical standpoint.

Also, the inspector observed whether the work was implemented

according to written instructions, and also evaluated quality

control involvement.

1)

Spray Chemical Addition Pumps, G 200 A&B

The inspector examined several In Service Testing (IST) records

of the spray chemical addition pumps. The pumps were rated to

deliver 0.4 gpm at 350 psi to the containment spray system,

when driven at a speed in the range of 77.5 to 155 rpm. In

order to meet the rated discharge, however, the pumps had been

run at considerably higher speeds of up to 193 rpm during

successive ISTs, dating back at least to June, 1986. As

explained in SCE Memorandum for File dated Dec. 1986, gradual

accumulation of "gases" (hydrazine vapor) in the pump cylinders

was- the cause and that running the pumps in the "unloaded"

21

state for some time would resolve the problem. This

explanation of the problem was provided by the vendor, Union

Pump Company. Since the pumps were positive displacement

pumps, it made.sense to the inspector that vapor accumulation

in the cylinders would reduce their discharge capacity, as well

as cause cyclic pressure fluctuations in the discharge piping.

The March, 1987 IST of pump G 200-A appeared to confirm this

diagnosis, during which the rated discharge was met while

running this pump at 143 rpm.

In all of the test documentation examined by this inspector the

reference- pressure has been stated as 315 psig, rather than the

rated 350 psig. The Technical Specifiations do permit

surveillance testing of these pumps at 90% of the rated

pressure. However, Article IWP-3100 of the ASME Boiler and

Pressure Vessel Code,Section XI, specifies 0.93-1.02 dP (where

dPr is the reference differential pressure) as the acceptable

range of suction/discharge pressure differential for IST of

pumps. Surveillance testing of the pumps at 315 psi discharge

pressure falls outside this range. Furthermore, the acceptable

range of flow range according to IWP-3100 is 0.94-1.02 Qr

(where Qr is the reference flow rate). The test flow rates

were slightly outside this range. These questions were raised

with licensee representatives and a verbal commitment was

obtained from the licensee to make a further engineering

evaluation of these pumps.

2)

Steam-Driven Auxiliary Feedwater Pump Modification

The steam-driven AFW turbine has had a history of repeated

tripping on overspeed, both when starting and while running.

The cause was determined to be slugs of condensed steam (low

energy water) from the supply pipe entering the turbine. The

realignment of the 3" steam supply line to give it a slope of

1/8" per 1'-0" to prevent accumulation of condensation appeared

to the inspector to be an adequate remedy.

The work-package contained adequate details of the work to be

performed, along with drawings and quality control hold points.

At the time inspection began, the steam supply line

modification had already been completed. Only the installation

of insulation back on the pipes remained. Interviews with

licensee representatives and those of the contractor (Bechtel),

and examination of the documentation indicated that adequate

quality control of the work had been implemented. No'

deviations or violations were identified.

3)

Charging Pumps, North and South

The inspector toured the charging pump area and examined

maintenance records relating to these pumps. MO No.

86032264000 required: installation of a "chicken feeder" and

associated piping to the south charging pump outboard motor

bearing. The chicken feeder was a gravity-fed oiler and 1/4"

22

supply pipe to the bearing. Under the section titled "Problem"

in the MO, no statement of the cause for malfunction of the

lubrication system was given, only instructions to install.

The licensee stated that the chicken feeder had been

inadvertently displaced by personnel working in the area. The

inspector noted that it is located in a restricted space of the

charging pump area such that it may be displaced down again.

No attempt at guarding against this possibility was apparent.

Installation of a simple wire-mesh guard would seem prudent.

4)

Other Pump Maintenance Activities

The inspector toured other pump areas and examined maintenance

procedures and documentation, including those relating to the

reactor coolant pumps B and C, the safety injection pumps E and

W, the feedwater pumps E&W, the motor-driven auxiliary

feedwater pump and the turbine plant cooling water pumps N and

S.

The inspector was satisfied with the licensee's actions in

these areas.

5)

Lubricant Storage Areas

The inspector examined lubricant storage areas in the Unit 1

Turbine Building and in a common storage area for all three

units. The latter was comprised of outdoor storage of

oil-drums and a large lockable cargo container. The inspection

was motivated by evidence of improper storage and labeling of

lubricants discovered by QA as far back as May, 1983 (CAR No.

S023-P-422, dated 5/1/83). A storage shed for proper storage

of the many types of lubricants used in the plant was planned.

This plan was postponed several times and the CAR is still

open. Meanwhile, licensee representatives stated that proper

labeling and protection measures from the weather has been

taken. The inspector toured the storage area to verify this

and found the conditions of storage, identification, and

labeling of lubricants acceptable. However the inspector noted

that the superior measure of a storage shed originally

proposed, and considered viable for almost 4 years, still

remained to be implemented, but there is no NRC requirement for

this.

6)

Fire Water Pump Diesel Tank Level Indicator

The inspector examined documentation regarding a deficient

Level gauge,.2/3 LG-5653 on the Fire Pump Diesel Tank, Units 2

and 3. The problems associated with this gauge have been cited

in at least 14 documents since July, 1984, including MO Nos.

85030006, 84000153001, 84110999, 85063049,.and 86010020 and

Non-Conformance Report No. 2-1652. While the level gauge has

been inoperable all this time, interim measures have been taken

to fabricate a sounding rod to provide a positive means of

level indication, which appears to increase the risk of

contamination of the fuel.

A Technical Specification violation

23

was avoided by keeping the tanks filled to 75%, vice the

required 65%. DCP/PFC 6630, dated 8/22/86 has been initiated

to replace the defective level gauge with sight glasses. At

the time of the inspection, the work remained incomplete.

No violations or deviations were identified.

d.

Mechanical Maintenance

The inspector observed mechanical maintenance activities on motor

operated valve (MOV) actuators; diesel generators (DGs); heating,

ventilation, and air conditioning (HVAC); pipe supports; and other

mechanical components. The activities were assessed to determine if

,the mechanical maintenance program is being implemented in

accordance with regulatory requirements and governing procedures and

instructions.

1) Motor Operated Valve Maintenance

Maintenance on motor operated valve (MOV) S1-RCP-MOV-18 was

observed by the inspector. The documentation for S1-RCP-MOV-19

was reviewed. The completed MO numbers for MOV-18 and MOV-19

were 87051647000 and 87051689000, respectively. Both of these

maintenance activities involved replacement of the torque

switch. Although the torque switches were still functional

the switches were replaced with a similar torque switch due to

problems with part availability of the older style of switch.

The switch was tested according to procedure S0123-I.8.313,

"Actuators - Motor Operated Valve Analysis and Testing System,

MOVATS". The procedure was adhered to and the content of the

procedure was found to be acceptable. The valve was observed

to be properly lubricated, with no foreign material observed.

The maintenance personnel were found to be knowledgeable on the

MOVATS system.

2)

Diesel Maintenance on Transamerica Delaval Incorporated (TDI)

Diesels

A portion of the preventative maintenance/surveillance

inspection of the TDI Number 2 Diesel was observed. The MO

number was 86111532000 and the procedure referenced was

S01-I-2.2, "Emergency Diesel Generator Surveillance

Inspection". The portions of the maintenance activity observed

were in compliance with the MO and the procedure.

A suggestion for procedural enhancement of S01-I-2.2 was made

by the inspector to the licensee. During observation of step

6.13.4, "Hot Web Deflection Measurement", it was noted by the

inspector that the gauge was brought to the temperature of the

engine, though the procedure does not make mention of this.

The concern was if the gauge was not brought up to the

temperature of the-diesel, the thermal expansion could cause an

erroneous reading. The inspector also observed that two

deflection gauges were used. The procedure implies that only

24

one gauge will be used. The licensee agreed to take these

suggestions for procedural enhancement and clarity under

consideration.

The inspector also observed tests performed by operations

personnel to verify operability.. Portions of the following

procedures were observed:

-

S01-10-1, "Diesel Generator Operations"

-

501-12.3-10, "Diesel Generator Load Test"

The TDI diesel performed a load rejection test (from 3000Kw)

without overspeeding. At the end of the load test, the

inspector was informed that the diesel was declared functional,

but was not declared operable due to operability concerns over

the vital station battery.

3) Diesel Maintenance on Dedicated Shutdown Diesels (DSD)

The DSD is used to power a third Auxiliary Feedwater (AFW)

Pump. This diesel was installed due to Appendix R (fire

protection) concerns relating to the loss of offsite power.

The observation of the running of this diesel was in

conjunction with an Integrated Surveillance Test on the AF

pump.

The inspector observed.that the startup of the diesel was in

accordance with procedure S01-10.7. The diesel was started and

tripped on low lube oil pressure. The inspector talked with

the craft people present and was informed that this trip was a

fairly common occurrence. The diesel was reset and started on

the second attempt. The inspector had concerns regarding the

operability of the diesel and talked with cognizant maintenance

personnel.. The inspector was informed that the sensing gauge

for the lube oil is at the end of the piping system, and it

takes time for the lube oil pump pressure to be seen by the

sensor. The inspector was also informed that a Startup Problem

Report (SPR) 6577 was written (4/1/87) describing this problem

and Station Technical had recommended some fixes to the problem

and an MO was currently being generated to repair it. The

inspector was also informed that, during emergency starts of

the diesel, this trip is bypassed. The actions taken by the

licensee were appropriate, and the inspector had no further

concerns regarding the operability of the DSD.

The DSD battery was also inspected. The battery was observed

to have 1/2 of a spacer plate missing between cells 58 and 59,

and some of the levels were slightly above the high level mark.

The inspector was informed that the spacer plate would be

replaced, and that procedure (SO1-I-4.14, "Battery Cleaning and

Watering") allows the level to be up to 1/4 inch above the high

level mark. The inspector was satisfied with the licensee's

0

response in

this. regard.

25

4)

HVAC Observations

The inspector walked down the Control Room Heating, Ventilating

and Air Conditioning (HVAC) system at SONGS 1. The purpose of

the control room HVAC is to limit the radiation and toxic gas

exposure to the control room operators during a design basis

accident.

The inspector had two concerns when inspecting the HVAC. One

concern was the covering of the HVAC ductwork by a taped

covering. This covering was to ensure system integrity. The

inspector was informed that this was a temporary measure and

was not a permanent fix to ensure system integrity. Another

concern involved-some HALON bottles secured near the HVAC

system air intake. The concern was that the HALON

concentration could be at unsafe levels if the tanks ruptured.

In discussions with the licensee, the inspector was informed

that the amount of HALON stored near the air inlet was not

sufficient to cause a health hazard. The inspector was

satisfied with this explanation.

5) Pipe Supports and Snubbers

The inspector performed a visual inspection of approximately

-two dozen pipe supports and snubbers on main feedwater, safety

injection, and diesel generator piping. The supports and

snubbers selected appeared to be installed in such a manner

that they could perform their intended function.

6) Other Mechanical Components

The inspector observed work that was being performed on several

mechanical components. The following MOs were observed in

progress:

87041416001, to install Grafoil sealant and place torquing

requirments on Conax connections to NAMCO EA120 limit

switches.

8705140000, to replace a leaking gas valve and 0-ring on

the accumulator for Safety Injection System (SIS) valve

S1-SIS-HV-851A

86110764001, to align "B" reactor coolant pump motor,

install the flywheel cover, and perform a test run with

the motor uncoupled.

The inspector considers that all work activities detailed on

these MOs were being performed in a satisfactory manner by

knowledgeable personnel. In addition, the inspector noted that

there was extensive involvement by QC inspection personnel

during performance of these MOs.

27

-

Configuration Control Procedure(s)

S0123-XIV-4.2, "Site Design Change Administration"

Modifications and design changes once approved by the plant

modification review committee are processed by engineering and

construction as a design change package (DCP). The design criteria

is developed through a series of design review meetings which

finally result in a design change package classified as Revision

"A".

This mile post is the first version of a design but is not yet

approved. In this form (Revision "A"), the DCP is routed to the

various groups such as station, operations, maintenance, quality

assurance, startup, etc. for their review and recommended

changes/input. Following this review, the DCP is revised to

incorporate those changes and issued as Revision "0".

Revision "0",

once approved, is the first working revision from which Construction

Work Orders (CWOs) are written to actually perform the work to

accomplish the modification/design change in the plant.

Following installation of the design change or modification,

component/system testing and preoperational testing takes place.

After preoperational testing is completed, the turnover package,

which includes all of the documentation from Revision "0" of the DCP

through the preopational test results and as built drawings, is

turned over to Quality Assurance (QA).

QA reviews the package to

determine that it is complete and that all QA requirements have been

satisfied. The turnover package is further reviewed by Station

Technical in parallel with station configuration control for

completeness. Following this review the as-built drawings are

released to operations for use in the control room and the package

is forwarded to Corporate Document Management (CDM) where it becomes

a permanent record of the plant.

b.

Review of Design Change Procedures and Construction Work

Orders

The inspector verified that the program for processing design,

design changes and modifications is functioning .in accordance with

prescribed procedures, and examined in detail the following Design

Change Packages (DCPs) which.were in various stages of completion.

Some of the DCPs were in configuration control indicating the

installation was completed and the turnover packages were in the

last review stage. For other DCPs, the installation was still in

process in the field or installation in the field had not yet been

started. The following DCPs were examined for authorization

signatures; safety, engineering, environmental, and ALARA

evaluations; drawing change authorization; QA review; as-built

drawings; completion signatures; etc.:

-

DCP-1-86-3072 Revision 0, Replace Magnecraft Relays In VR

Transfer Scheme With Electro Switch Lockout Relay

-

DCP 1-85-3303.0 Revision 1, Valve Operation Modifications

28

-

DCP 1-87-3391, Provide Duct Heaters for the Control Room

Emergency HVAC System

-

DCP 1-85-3009-1, Install Switchgear Enclosure Foundation Floor

Slab

DCP 1-85-3009.5, Dedicated Shutdown System/Appendix R

Modifications

-~

DCP 1-85-3009.9, Modification and Relocation of Dedicated

Shutdown Panel C-38

-

DCP 1-85-3009.14, Dedicated Safe Shutdown Water and Fuel Makeup

In addition, the following Construction Work Orders (CWOs) for the

field installation of the Design Changes and Modifications, for the

above DCPs, were examined in detail by the inspector for proper

authorizing signatures, QC participation, job completion sign-off,

final QA review, etc.:

-

CWO 87030454000, install roto hammer remote extensions for

valves VCC-324 and VCC-405 in accordance with FIDCN M-4743 and

M-4769.

CWO 87030382000, add two coredrills to concrete roof on reactor

auxiliary building in accordance with FIDCN C-2151.

CWO 87030892000, relocate valve VCC-324, add valve VCC-405 and

delete valve FV-3079 in accordance with FIDCN M-4743.

CWO 87030373000, install cables 1GHED9RP1, C1, I and terminate

them at GEO9RY.

CWO 8703040900, grout any misdrilled holes resulting from

installation of conduit 73471G and relay box GEO9RY.

CW087022396000, install relay cabinet GEO9RY and conduit 73471G

for LV exciter cabinet for DG2.

CW08704298000, replace relay GEO9RY per NCR-S01-P-6104.

CWO8704302300, perform inspection and take baseline data on

replacement LOR/ER relay in accordance with test procedure

S0123-II-11.152.

-

CW087041288000, perform inspections and take baseline data on

new LOR/ER relay as required per instrument and test procedure

50123-I-11. 152.

-

CW087020803000, test LOR/ER relays in E09 Auxiliary Panel

GEO9RY, perform circuit tie-ins INEO9, low voltage excitation

panel, retest circuits in accordance with SO123-II-11.152.

29

The above documentation (DCPs and CWOs) appeared to be in order and

processed in accordance with applicable procedures.

Two DCPs were selected to inspect in the field to verify the

installation of the design changes and modifications. A walkdown

was made in the charging pump area to inspect completed

modifications made to two remote valve operators under DCP

1-85-3303.0, valve operator modifications. The .in

process work of

installation of a switch on a panel in the control room was

inspected. This-installation was being accomplished under DCP

3465.0, Vital Bus No. 4 Transfer. These installations appeared to

have been made or were being made in accordance with prescribed

design and CWOs.

c.

Audit Reports

Further verification of the licensee's program for design, design

changes and modification included examining the following three

audits conducted in this area by the licensee:

1) SCE-2-86/FCR-1-86, conducted February 1986

The purpose of this special audit was to assess the

effectiveness of the application of the quality assurance

program to the design and procurement processes for the Diesel

Generator in the Dedicated Safe Shutdown System for San Onofre

Unit 1.

2)

SCES-027-86, conducted June/July 1986.

The purpose of this audit was to verify Project/Startup

Engineering implementation of the applicable requirements

specified in Chapter 2-A, "Design Development, Review and

Approval" of the Topical Quality Assurance Manual (TQAM), E&C

24-10-16, "Development, Review, Approval and Release of SCE

Design Change Packages (DCPs) SONGS 1, 2 & 3 and Administrative

Procedure (AP) No. 10, "Design Change Process".

3)

SCE-22-86, conducted August 1986.

This audit covered selected review of SCE design change

packages and field generated interim design change notices.

The audits appeared to be comprehensive in the areas examined and

demonstrates the effectiveness of QA's involvement in the licensee's

program for design changes and modifications.

The inspector in his examination of the licensee program for design,

design changes and modifications reviewed the licensee's annual report

dated June 11, 1986 of facility changes including a summary of the safety

evaluation for each change/modification. The report included only two

facility changes for 1986; 1-85-3066.0 and 1-85-3055.1. Both changes

involved replacement of environmentally unqualified containment

electrical penetrations and safety related cables. The report and safety

.

3 0

evaluation summaries appeared to be adequate and to satisfy the

requirements of 10 CFR 50.59(b)(2).

It appears from examination of the above documentation and the field

inspections that the procedures prepared to describe the functioning and

manage the licensee program for design, design changes and modifications

have adequate controls to ensure a proper operating program.

No violations or deviations were identified.

11. Radiological Controls

The inspector reviewed the following areas: audits, changes in

organization and programs, training and qualification of personnel,

external and internal exposure, maintaining occupational exposures ALARA,

and control of radioactive material.

This included reviews of licensee

records and reports, discussions with licensee and contract personnel,

and several tours of the the licensee's facility.

The inspector reviewed Quality Assurance Audit SCES-020-86 and various

Field Surveillance Reports as applicable to the Unit 1 mid-cycle outage.

The deficiencies identified appeared to have been adequately addressed

and corrected. The inspector observed that the audit team included

individuals qualified as lead auditors in the area of radiological

controls as defined in ANSI/ASME N45.2.23-1978, "Qualification of Quality

Assurance Program Audit Personnel for Nuclear Power Plants."

The inspector interviewed the Unit 1 Health Physics (HP) supervisor, the

Unit 1 Radioactive Material Control (RMC) General Foreman, the RMC

Manager, and various HP and RMC leads and technicians in regard to the

preparations made for the.Unit 1 outage and significant changes

implemented since the last inspection. The inspector was informed that

the Unit 1 HP Supervisor had been recently appointed to that position.

The inspector was also informed that a significant effort had been made

at the start of the outage by the RMC organization to decontaminate the

42 and 31 foot levels of the Unit 1 containment building. This resulted

in entry to these levels, as well as a few areas of the 22 foot level, in

street clothes. Several supervisors interviewed by the inspector

commented that the decomtamination resulted in easier access to the work

area and, they felt, more frequent supervisory tours.

The inspector-was informed by the HP Supervisor and the RMC Manager that

30 and 47 temporary technicians had been added to their respective staffs

to support the outage. The inspector examined the resumes of select

temporary contract HP journeyman technicians and all appeared to meet the

requirements of ANSI/ANS-3.1-1981, "American National Standard for

Selection, Qualification and Training of Personnel for Nuclear Power

Plants."

The inspector reviewed several contract HP technician

Qualification Manuals and all appeared to be appropriately complete. The

inspector discussed with the RMC Manager and General Foreman the training

of RMC technicians with regard to the Unit 1 decontamination effort and

outage. The inspector was informed that temporary Unit 1 RMC

decontamination personnel had received on-the-job training at Units 2/3

two weeks previous to the start of the outage to familiarize personnel

31

with the decontamination techniques to be used and that they also had

received "weight" training to familiarize them with the proper methods

for lifting and carrying heavy items.

The inspector made several tours of the Unit 1 containment building and

observed numerous jobs in progress, particularily:

Reactor Coolant Pump Repair andReassembly

Excore Detector Changeout

Reactor Cavity Inspection

Equipment Decontamination

Upender Cavity Sludge Removal Preparations

The inspector observed that the workers were wearing appropriate

dosimetry, anti-contamination clothing, and respiratory protection (as

required by their respective REPs) and appeared to be expeditiously

carrying out their tasks. The inspector reviewed current exposure data

for personnel involved in the outage and noted that there were none in

excess of the 900 millirem whole-body SCE administrative limit but that

five workers had received exposure extensions. The inspector reviewed

the five respective Radiation Exposure Limit Extensions and noted that

they appeared to be complete, properly reviewed and signed, and each

included a correctly completed SCE Occupational External Radiation

Exposure History which had information equivalent to that contained on

Form NRC-4. During the tours the inspector also noted that plant areas

appeared to be appropriately posted and that containment housekeeping

appeared to be in good order. The inspector was informed that there were

no known exposures of personnel to airbourne radioactivity in excess of

the 30 MPC-hr administrative limit nor had there been any positive

whole-body counts attributable to the intake of radioactive material at

the site during the outage.

The inspector was informed that Irradiated Fuel Fragment controls had

been instituted for select jobs but that none had been found in systems

with the exception of one highly radioactive Co-60 particle which had

been removed from the Radioactive Waste Storage Tank. The particle was

noticed when a survey of the outside of the tank, after a flush of a hot

spot on a Reactor Coolant loop drain line, revealed a 1000 R/hr hot spot

on the bottom of the tank. The particle was removed by a special

procedure and was in storage at the time of the inspection. The particle

was observed to be about the size of a grain of sand. Four other

discreet particles had been found during the outage at Unit 1 but were

not associated with.plant systems. The inspector was informed that there

had been 45 personnel contamination events to date during the outage and

that 18 of these had occurred during the containment decontamination

.process.

The inspector reviewed notations of calibration and performance checks on

portable survey instruments and noted some minor discrepancies with the

notation of performance check dates which were pointed out to the

cognizant HP personnel and expeditiously corrected. The inspector

observed personnel frisking with both hand-held friskers and the

beta-booths. Personnel appeared to be frisking properly and personnel

contamination alarms seemed to be properly responded to and documented.

32

The inspector toured radioactive material storage and processing areas at

Units 1 and 2/3. The compressible waste generated at Unit 1 was being

transferred to Units 2/3 for compaction.

During a tour of the radioactive material storage area on the east side

of Units 2/3 the inspector noted eight gray boxes, approximately

3'x3'x5', in the area outside door R3-60. The boxes bore the required

"Caution-Radioactive Material" label but no information was provided on

the label as to what radiation levels were present or what material was

contained in the boxes. The area was posted as a Radiation Area but the

boxes were stored in a housekeeping area separate from the normal RMC

storage. Readings taken by the inspector on June 3, 1987, with an

Eberline model .RO-2 ionization chamber, serial number 897, calibrated on

March 24, 1987, and due for calibration on June 24, 1987, indicated a

maximum contact dose rate of 48 mrem/hr and a general area dose rate

around the boxes of 5-10 mrem/hr. These dose rates were markedly higher

than others in the general area.

The inspector brought this to the attention of the Units 2/3 HP

supervisor and inquired if the noted labelling was sufficient to meet the

requirements of Health Physics Procedure S0123-VII-7.4, "Posting and

Access Control," and 10 CFR 20.203, "Caution signs, labels, signals and

controls."

The supervisor stated that he felt that the current

labelling was not sufficient to meet the requirements. The supervisor

later informed the inspector that the boxes had been surveyed and

appropriately labelled with the box contents and radiation levels. The

supervisor stated that previously made documented surveys of the loaded

boxes were not available. The inspector was informed by the HP Manager

that the boxes contained Reactor Coolant Pump Seals in storage casks.

The Manager stated that the labelling of these boxes with only the

radiation symbol and the words "Caution-Radioactive Material" was not

sufficient to meet the requirements of HP Procedure S0123-VII-7.4, that

the vast number of packages containing radioactive material at the site

were properly labelled and that these must have been missed as the

packaging and movement had been completed at the time of shift turnover

on June 1, 1987.

Technical Specifications, Section 6.11, Radiation Protection Program,

reads:

Procedures for personnel radiation protection shall be prepared

consistent with the requirements of 10 CFR Part 20 and shall be

approved, maintained and adhered to for all operations involving

personnel radiation exposure.

Health Physics Procedure 50123-VII-7.4, paragraph 6.1.2.6, "Radioactive

Materials Container," requires that:

Each container having radioactive material in excess of the amounts

specified in Appendix C of 10 CFR 20 shall bear a durable, clearly

visible label bearing the radiation caution symbol and the words:

0II

33

"CAUTION, RADIOACTIVE MATERIAL"

OR

"DANGER, RADIOACTIVE MATERIAL"

It shall also provide sufficient information to permit individuals

handling or using the containers or working in the vicinity thereof

to take precautions to avoid or minimize exposures.

A similar violation involving the labelling of two 55 gallon drums was

noted in November, 1986, and documented in inspection report number

50-206/86-42. Failure to adequately label the eight Reactor Coolant Pump

Seal boxes is a violation of the requirements of Technical Specifications

(87-05-07).

The inspector interviewed the cognizant ALARA engineers and reviewed the

ALARA program planning and execution for the Unit 1 outage. An outage

goal of 80 person-rem had been set of which 67 person-rem had been

expended by the 27th day of the 45 day outage. The inspector reviewed

select Radiation Exposure Permits, Maintenance Orders, ALARA Job Reviews,

Temporary Shielding Authorizations, Surveys, and the special procedure

for the hot particle removal from the Reactor Coolant Drain Tank. The

inspector noted that there had been a significant increase in the number

of Maintenance Orders issued for the outage over the number planned, an

increase from approximately 400 to approximately 650, and that there had

been an increase in the scope.of work on let-down valves in the vicinity

of the non-regenerative heat exchanger. It appeared that the outage

exposure goal might be exceeded but the level of effort and involvement

of the ALARA group appeared significant. Indeed, the setting of a

seemingly agressive exposure goal and the daily participation of the

ALARA group in work planning and execution appeared to be effectively

maintaining occupational exposures as low as reasonably achieveable.

Within the area inspected, one violation was identified.

12. Followup of Inspector Identified Items

a.

(Closed) 50-206/86-43-01 -

Safety Injection/Feedwater Pump Bearing

Oil Supply

This item dealt with several concerns regarding safety injection/

feedwater (SI/FW) pump bearing oil supply.

1) One aspect concerned the ability of the installed flow meter to

indicate flow at the reduced levels resulting from

reinstallation of flow orifices. The licensee replaced the

flow meter with one more suited to measure the existing flow

levels per Maintenance Order (MO) 8611340000.

2) The inspector requested the licensee confirm the proper

operation of the pump bearing temperature monitor and alarm.

This was completed by the licensee per MOs 93111610002 and

86111207000.

34

3)

The inspector requested the licensee confirm proper oil flow to

the motor bearings. This was completed by the licensee as

specified in MOs 86111166000 and 86111051001.

4) The inboard motor bearing lube oil sight glass appeared cloudy.

The inboard sight glass was replaced with the outboard sight

glass and a new sightglass was installed in the outboard

position. This was accomplished per MO 86100605000.

The inspector found the licensee's actions concerning this item to be

acceptable and it is closed.

b.

(Closed) 50-361/86-25-03 Procedures and Training on AFW

Tappet Relatch

This item involved a finding by the previous Region V team

inspection with regard to the method for resetting the auxiliary

feedwater (AFW) pump turbine overspeed trip.

Procedure S023-2-4 has been revised in accordance with TCN 9-4 to

include resetting of the P-140 turbine overspeed trip by ensuring

actuator HV-4716 is fully closed and pulling the trip lever

connecting rod towards HV-4716.

The inspector briefly interviewed a representative sample of Nuclear

Plant Equipment Operators (NPEOs) to ensure that they had knowledge

of this reset procedure. Also, the inspector observed signs,

located in the area of the AFW pumps, with detailed diagrams as to

how to reset the P-140 turbine overspeed trip.

The licensee appeared to.have addressed this item adequately and it

is closed.

c.

(Closed) 50-206/82-26-01 -

ORMS Low Flow Alarms Unexplained on

Channels 1211 and 1212

This item concerned the background count rate on Operational

Radiation Monitoring System (ORMS) channel 1211 which had a

background count rate of 35,000 CPM. This was 15,000 CPM above the

alarm setpoint specified in procedure 501-1.3-1. Also, channels

1211 and 1212 were selected to monitor the stack instead of

containment. The licensee made this selection because a low flow

alarm was received whenever the channels were selected to monitor

the containment.

Procedure S01-2.2.1 was revised to specify that the alarm setpoints

for these channels are determined by the Chemistry Department and

are periodically reviewed and revised as necessary by Chemistry.

Also, spurious low flow alarms from channels 1211 and 1212 have been

eliminated. The inspector personally inspected these channels in

the control room which were selected to monitor containment and no

low flow alarm was present. Further, in order to ensure that

Technical Specification requirements are met, these channels are

'~

'

'

35

normally selected to monitor containment. The shift superintendent

stated that he has not observed any spurious low flow alarms from

these channels. Therefore, this problem is considered resolved and

this item is closed.

d.

(Open) 50-206/86-11-01:

Safety Analysis and ASME Section XI

Operability Limits for Inservice Testing of Pumps

During this inspection, the licensee provided copies of memoranda

between P. A. Croy and J. L. Rainsberry regarding:

(1)

determination of FSAR design requirements for those pumps tested in

the inservice testing program, and (2) the acceptance criteria

delineated in the inservice testing program. The two sets of pump

requirements were summarized in a memo from P. A. Croy and B. L.

Woods dated December 17, 1986.

However, the methodology used to

assess the appropriateness of the IST pump acceptance criteria was

not clear. The individual who prepared the comparison document was

unavailable for interview during the entire course of this

inspection. Therefore, the validity of the comparison was not

verified by the inspector. This item remains open pending review

and discussion between the cognizant licensee individual and an

inspector.

e.

(Open) 50-361/85-22-03:

Safety Analysis and ASME Section XI

Operability Limits .for Inservice Testing of Pumps

This item is identical to the item discussed immediately preceding

except that it applies to Unit 2. This item remains open pending

review and discussions between the cognizant licensee individual and

an inspector.

f.

(Closed) 50-206/86-34-01:

Evaluate Need for Additional Licensee

Actions on Testing Foxboro Controller Wire Harnesses

While evaluating the I&C maintenance program, the status of this

open item concerning the degradation of Foxboro wiring harnesses was

reviewed. Forty (40) MOs were generated to replace the Foxboro coil

cords. Of these forty MOs, eight (8) were reviewed in detail. The

detailed reviews included field observations of the preparatory

bench work and the in-plant installations of the hardware. It was

found that not all of the MOs had been completed and released to

document-control, but most of the actual work of installing the

replacement cables had been completed.

The eight MOs for performing inspection, testing, or installation of

the Foxboro equipment which were examined are as follows:

86090856000

86090857000

86090858000

86120839000

86120846000

86120853000

36

86120865000

86120869000

Based on the evaluation of the Foxboro related MOs and the work

completed at the time of the inspection, actions are being taken by

the licensee to replace the Foxboro coil cords. Therefore, this

item is closed.

13.

Exit Meeting

On June 12, 1987, an exit meeting was held with the licensee

representatives identified in paragraph 1. The inspectors summarized the

inspection scope and findings as described in this report.