ML13316C019

From kanterella
Jump to navigation Jump to search
Insp Repts 50-206/89-11,50-361/89-11 & 50-362/89-11 on 890313-17 & 0403-07.Violation Noted.Major Areas Inspected:Qa Program Implementation,Design Changes & Mods,Inspector Followup Items & Followup on Items of Noncompliance
ML13316C019
Person / Time
Site: San Onofre  Southern California Edison icon.png
Issue date: 05/25/1989
From: Caldwell C, Johnson P
NRC OFFICE OF INSPECTION & ENFORCEMENT (IE REGION V)
To:
Shared Package
ML13316C017 List:
References
50-206-89-11, 50-361-89-11, 50-362-89-11, GL-83-18, GL-88-14, NUDOCS 8906090077
Download: ML13316C019 (15)


See also: IR 05000206/1989011

Text

U. S. NUCLEAR REGULATORY COMMISSION

REGION V

Report No.

50-206/89-11, 50-361/89-11, 50-362/89-11

Docket No.

50-206, 50-361, 50-362

License No.

DPR-13, NPF-10, NPF-15

Licensee:

Southern California Edison Company

P. 0. Box 800, 2244 Walnut Grove Avenue

Rosemead, California 92770

Facility Name:

San Onofre Units 1, 2, and 3

Inspection at:

San Onofre, San Clemente, California

Inspection conducted:

March 13 through 17 and

April 3 through 7, 1989.

Inspector:

,_

_

_

_

_

_

_

_

_

C.f. Caldwe, Project Inspector

Date Signed

Approved By:

,.* o sn

1:4

P.H. Johnson, Chief,

Date Si ned .

Reactor Projects Section 3

I nspection Summary:

Inspection on March 13 -

March 17,

1989 and April 3 -

7, 1989 (Report

No. 50-206/89-11) 50-361/89-11, 50-362/89-11

Areas Inspected:

Routine unannounced regional inspection of licensee QA

program implementation, design changes and modifications, inspector followup

items, and followup on items of non-compliance.

Inspection procedures 35502,

37700, 92701, 92702, and 30703 were covered.

8 9 0

6 0 9 0 0 7 7 g 0 ,

PNu

Safety Issues Management System (SIMS) Items:

None

Results:

General Conclusions and Specific Findings:

In general, the licensee's program enhancements for quality oversight

groups were being implemented and showing a positive trend. However, the

inspector considered that additional reviews of quality oversight group

activities were necessary to verify that program enhancements were

effective.

Significant Safety Matters:

A concern was identified with the performance of reviews 'conducted in

accordance with 10 CFR 50.49 as related to the evaluation of the effect

on operation of the plant with inoperable excore neutron monitors during

post accident conditions.

Summary of Violations:

One violation of NRC requirements was identified (Paragraph 4.a) dealing

with the adequacy of the licensee's corrective actions to resolve a

10 CFR 50.49 equipment qualification discrepancy.

Open Items Summary:

One unresolved item was identified (Paragraph 4.a) with regard to lack of

the Updated Final Safety Analysis Report and the control panels to list

the source range loc power instruments as post accident monitoring

instrumentation. One followup item was identified concerning

implementation of independent safety engineering group review of

nonconformances. In addition, four followup items, one unresolved.item,

and one 10 CFR Part 21 report were closed.

DETAILS

1. Persons Contacted

Licensee Personnel

  1. H. E. Morgan, Station Manager

R. M. Rosenblum, Quality Assurance Manager

  1. R. W. Krieger, Operations Manager

V. B. Fisher, Unit 2/3 Superintendent

  • M. L. Merlo, Manager, NEDO
  • D. A. Herbst, Manager, Site QA
  • M. P. Short, Project Manager, DBD
    • L. K. Carlisle, Nuclear Engineering Supervisor
    • R. D. Plappert, Compliance Supervisor
  1. W. W. Strom, Supervisor, Independent Safety Engineering Group
  1. L. D. Brevig, Supervisor, Onsite Nuclear Licensino
  1. R. A. Neal, Senior Engineer 2
  1. S. J. Foglio, Engineer 2

,#G. T. Gibson, Onsite Nuclear Licensing

  • C. A. Couser, Onsite Nuclear Licensing
    • R. L. Baker, Onsite Nuclear Licensing
  1. D. A. Werntz, Compliance Engineer
  1. K. D. Flynn, Engineer 1
  1. J. H. Martin, Engineer 1
  • Denotes those attending the exit meeting of March 17, 1989.
  1. Denotes those attending the final exit meeting on April 10, 1989.

The inspector also contacted licensee operators, ehgineers, technicians,

and other personnel during thecourse of the inspection.

2. Evaluation Of Licensee Quality Assurance Program Implementation

(35502)

The purpose of this review was to evaluate the effectiveness of the

licensee's implementation of the quality assurance program and to

recommend, based on this evaluation, changes to the current level of

inspection effort in this area.

This effort consisted of a comprehensive

review of program surveillances and discussions with Southern California

Edison's (SCE's) quality oversight groups in order to determine if recent

changes in personnel and program direction were enhancing the

effectiveness of the quality programs to find problems and weaknesses in

SCE activities. During this inspection, the licensee's operating

experience review (OER) program and activities performed by the

independent safety assurance group (ISEG) were not reviewed. In

addition, QA audits were not reviewed during this inspection since the

licensee had not finalized any.audits for issue under the revised program

format.

Surveillances Reviewed

The inspector reviewed 20 recent surveillances that were performed of

maintenance, surveillance, and operational activities including the

fol 1

owi no:

2

-

SOS 13-89, "Technical Specification Section 4.10.A Verification"

-

SOS 29-89, "Removal Of Temporary Facility Modifications"

-

SOS 59-89, "Verify Actions In Response To 10 CFR 21 Report"

The inspector noted that most of the surveillances had findings of minimal

significance. However, several of the surveillances had substantive

findings regarding activities conducted in the plant. For example, in

SOS 89-13, personnel found that several welds that should have been

inspected during the current Unit 1 outage were not scheduled. As a

result of the finding, a corrective action request (CAR) was prepared.

Other examples were SOS 29-59 in which personnel found a support rail

that was bent out of position which would prevent a breaker from closing

and SOS 59-29 in which a procedure was found that had not been updated.

The review of surveillances indicated that the reports were more detailed

than in the past.

The inspector also discussed a recent significant surveillance findings

concerning pressurizer power operated relief valve (PORV) setpoint on

Unit 1. In particular, during a surveillance to review the stroke time

of the PORVs, QA personnel found that the stroke time for one of the

PORVs was slightly greater than the design requirement. In addition,

personnel found that the PORV setpoint for the overpressure mitigation

system and Technical Specification 3.20 had not been revised to reflect

the latest changes to the heatup and cooldown curves.

As a followup to this

finding, the licensee was evaluating the condition for safety

significance and additional corrective actions.

Principal Enhancements To Increase Quality Oversight Effectiveness

As a followup to discussions held during recent management meetings,.the

inspector discussed QA and other quality oversight program.changes with

responsible personnel.

The inspector noted that the licensee had

established or was in the process of establishing a number of program

enhancements.

Some of the more noteworthy changes were as follows:

-

Area Monitoring Program - This program was upgraded to provide the

nuclear oversight organization (all groups except for QC) with a

systematic method for direct observation of-the implementation of

established QA program requirements (e.g., housekeeping, material

conditions, and temporary modifications).

-

Quality Assurance Monitoring Report - This program was established

as an activity oriented program similar to surveillances. The

principal difference was that no paperwork reviews were done. This

report was developed to provide a method for observing plant

activities and documentation of the observations in a more efficient

manner.

-

Manpower Utilization Program -

The licensee was developing upgraded

standards and a certification process for QA personnel.

These

upgraded standards will consist of an annual requalification process

(with requirements exceeding the American National Standards Institute

3

(ANSI) standards).

The process will require a minimum number of

audits to be performed within a given period to maintain

qualification. In addition, personnel will be required to take a

requalification examination and review by a qualification board.

-

QA/QC Training - The licensee was developing a training program in

accordance with the Institute For NuclearPower Operations (INPO)

guidelines.

-

QA Audits - The licensee revised the format for audit performance so

that future audits will be more performance based (e.g., similar to

the new NRC inspection program).

-

Proactive Evaluation/Engineering Review (PEER) Program For Design

Change Documents - This program was instituted to provide the QA

organization with more effective measures to evaluate design change

documentation prior to approval.

Design Changes -

The procedures were revised to require that design

changes undergo review and comment prior to issue.

Officers' Council Weekly Progress Report On Quality Assurance -

The

licensee established this program to issue a weekly progress report

identifyinq QA actions/findings associated with recent audits,

surveillances, and other quality oversight group activities. Part

of the intent of issuing these reports was to detail issues in

such a mariner thatproper management attention could be focused to

resolution of the items.

The inspector reviewed the reports for the

weeks of March 2, 1989 through March 16, 1989.

The inspector noted

that several significant issues had been identified in the reports

for resolution. For example, one audit identified that functional

testing at end-of-discharge voltages for the Unit 1 motor operated

valve inverters and Unit 2/3 shutdown cooling valve inverters had

not been performed. As a result of this finding, the licensee

issued two nonconformance reports to evaluate the conditions.

Trending - The licensee was developing a "real time" trending

program for audits, surveillances and other quality findings.

This

program will primarily be used for trending and feedback for the

quality oversight groups.

QA Organization Employee Advancement Program -

The licensee

established this program to define a career path for employees that

details the requirements for advancement. This will include

opportunities to broaden the experience base through

inter-department cross-training.

Commitment Tracking System

The inspector selected several licensee commitments to ensure that the

licensee's system for tracking commitments was functioning properly.

The

inspector selected four commitments as follows:

4

-

Limitations placed on the six-inch vent valves in the containment

venting and purging system (Ref. letter to SCE dated November 2,

1984).

This item was identified in the San Onofre Commitment

Register (SOCR) as number 8402069/001.

-

Final report on fire protection Technical Specification changes

This item was identified in the licensing tracking list with a due

date of March 31, 1989.

-

June 17, 1988 amendment application additional information -

This

was identified in SOCR as number 8800295/001 with a due date of

March 31, 1989.

-

Response to Generic Letter 88-14 -

This was identified in SOCR as

item number 88120291/001 with a due date of May 19, 1989.

The inspector noted that these items were being tracked by the licensee

and considered that based upon this review, the licensee's tracking of

commitments was adequate.

Summary

Based upon the documents reviewed and discussions held with SCE

personnel, the inspector considered that the licensee's quality oversight

groups were headed in a positive direction. However, the inspector

considered .that it was .too early to tell if the oversight groups were

fully effective in evaluating licensee programs. The recent enhancements

provided evidence that SCE was being responsive to past NRC concerns.

The inspector considered that the true test of the effectiveness of the

quality oversight organizations would be the ability to track and resolve

recurring deficiencies, a continued reduction in the backlog of

corrective action followup items, and more QA involvement to identify

problem precursors before they reach NRC attention and concern. The

inspector will continue to review the licensee's implementation of

program upgrades to enhance quality oversight group effectiveness during

future inspections.

No violations or deviations were identified.

3.

Design, Design Changes, And Modifications

(37700)

The inspector reviewed several design changes and modifications that were

determined by the licensee to not require approval by the NRC. This was

performed in order to determine if these actions were done in conformance

with the requirements of Technical Specification (TS) 10 CFR 50.59, the

Safety Analysis Report, and the licensee's Quality Assurance Program.

The inspector reviewed the following proposed facility changes (PFCs):

-

PFC 3-87-6554.17, Revision 0, that was issued to provide an

alternate power source to the excore neutron monitoring system for

Unit 3.

-

PFC 1-88-5113.2, Revision 1, that was issued to install a 480 volt

switchgear bus-tie breaker trip on safety injection/loss of off-site

power for Unit 1.

5

PFC 2-87-6604, Revision 0, that was issued to modify the Unit 2

remote shutdown panel to bring it in compliance with the present

requirements of NUREG-0700.

PFC 2/3-87-6554.02, Revision 0, that was issued to install eight

hour emergency lights in Units 2 and 3 for Appendix R compliance.

-

PFC 1-88-5113.04, revision 0, that was issued to add an automatic trip feature for the station service transformer number three supply

breaker in Unit 1.

-

PFC 2/3-84-238, Revision 0, that was issued to add an air motor

start counter and other equipment to monitor diesel generator start

times in Units 2 and 3.

-

PFC 1-88-3410.0, Revision 2, that was issued to install level

switches at the Unit 1 refueling water storage tank.

-

PFC 1-88-3496.0, Revisiun 0, that was issued to replace the existing

Unit 1 feedwater/stem flow computer and mismatch comparator with

qualified equipment.

The inspector noted that these PFCs contained the necessary reviews and

approvals prior to issue to the station including nuclear safety group

(NSG) reviews. In addition, the inspector noted that reviews required by

10 CFR 50.59 were performed and that other considerations such as "As Low

As Reasonable Achievable (ALARA)," and fire protection were performed.

The inspector also rioted that the licensee had prepared maintenance

orders to implement the PFC/DCPs and that these maintenance orders were

properly controlled. Additional reviews of the licensee's program for

design changes and modifications will performed during future

inspections.

No violations or deviations were identified.

4.

Licensee Action On NRC Inspection Findings

(92701)

a.

(Closed) Followup Item (361/88-28-01), "Review Acceptability

Of Safety Evaluation For Gamma-Metrics Connectors"

This item identified a concern with regards to the licensee's safety

evaluation and decision to "accept-as-is" Gamma Metrics cable

connectors used on the startup log power excore neutron monitors.

On February 19, 1988, Gamma-Metrics issued a 10 CFR Part 21

notification of a potential deviation in which the connector solder

joints could leak at elevated temperatures.

The connectors were

used in Units 2 and 3 excore monitoring systems.

In this Part 21

report, licensees were requested to send spare connectors to the

vendor for testing. SCE complied with that request and sent one

connector that was located in stores. The vendor tested connectors

that were sent and revised their Part 21 report as a result of the

failures that were found.

On May 10, 1988, the vendor sent a second

letter that stated the following:

"The results of these tests

convince us that there is a significant possibility of having leaks

in cable assemblies which are installed in our customers'

6

facilities."

The vendor also stated that a leak in the cable

assembly could cause the neutron flux monitoring channel performance

to be degraded or to fail during a design basis accident.

As a result of the Part 21 report, SCE issued nonconformance report

(NCR) G-0865, Revision 0, to identify that there was a possible

problem with solder connections on Gamma-Metrics cable assemblies.

The NCR stated that the equipment was operable and that the

condition was not reportable. The interim disposition of this NCR

was to "accept as-is" per the attached safety evaluation, and the

final disposition was to rework or retest the connectors when the

qualified unit was supplied by the vendor. The inspector reviewed

the safety evaluation for the NCR that was prepared by station

technical.

It stated that there was no nonconforming condition

since the vendor tests only raise the possibility of leaks at the

solder joints.

The licensee's nuclear engineering group also

provided input (disposition and 10 CFR 50.59 evaluation) to this NCR

in a communication dated July 25, 1988. In that communication, the

engineering organization dispositioned the NCR by identifying that

the condition was not a problem since there were two redundant

trains and both would have to fail in order for the system to be

completely nonfunctional. In addition, engineering considered that

if the excore neutron monitoring system were to fail, there were

alternate monitoring means to assess core reactivity such as the

following:

1. Reactor coolant system (RCS) hot and cold leg temperature

difference.

2. Control element assembly bottom contact indicators

3. Boronometer readings.

4. RCS sample analysis.

The inspector questioned the evaluations that were performed by

station technical and the engineering organizations. In particular,

the inspector had the following concerns:

-

It did not appear that the post accident monitoring function of

the excore neutron monitors was fully considered when the

licensee evaluated them as operable.

-

The station technical safety evaluation stated that there was

no nonconforming condition despite the fact that the vendor

indicated that there was a significant possibility of having

leaks in the installed cable assemblies.

-

The licensee did not query the vendor to sufficient detail to

determine the extent of failures of the tested cable assemblies

or obtain other detailed information to aid in the operability

assessment.

-

The engineering disposition considered that the connector

problem was very significant since both trains of the excore

neutron monitors would have to fail in order for the system to

be completely nonfunctional.

This was despite the fact that

7

the vendor had identified the potential common mode failure of

the connectors.

The four alternate means of verification (mentioned above) were

not in themselves adequate to determine core reactivity during

a design basis accident. Regulatory Guide 1.97, Revision 2,

"Instrumentation For Light-Water Cooled Nuclear Power Plants To

Assess Plant And Environs Conditions During And Following An

Accident" reinforced this position by detailing the

requirements for post accident monitoring (PAM) equipment. In

particular, it defined Type A variables as those variables that

provide primary information needed to permit the control room

operating personnel to take specified manually controlled

actions for which no automatic control is provided. It also

placed these variables into three Categories to establish

further requirements for them (1 - highest, for key variables,

and 3 - lowest). Regulatory Guide 1.97 classified the excore

detectors as a Category 1 variable and Edison classified them

as a Type A variable. None of the alternate means of

verification listed by the licensee were classified as Type A

variables in the Regulatory Guide. They were identified as

verification variables only.

The licensee did not notify the control room operators that

there was the potential for inaccurate indications should

degradation of the connectors take place during a design basis

accident (DBA).

Consequently, the inspector considered that

the operators could make a judgement or take some action with

erroneous-or even a complete lack of information as to core

reactivity.

10 CFR 50.49 established requirements for the qualification of

electrical components important to safety. Paragraph 50.49(f)

requires that each item of electric equipment important to safety

must be qualified.

In addition, paragraph 50.49(j) requires that a

record of the qualification must be maintained to permit

verification that each item of electric equipment important -to

safety is qualified for its application and meets its specified

performance requirements when it is subjected to the conditions

predicted to be present when it must perform its safety function.

The NRC expanded equipment qualification policy by issuance of

several Generic Letters (GLs) including GL-88-07, "Modified

Enforcement Policy Relating to 10 CFR 50.49." This GL states that

when a potential deficiency has been identified by the NRC or

licensee in the environmental qualification of equipment, the

licensee is expected to make a prompt determination of operability

(i.e., the system or component is capable of performing its intended

design function), take immediate steps to establish a plan with a

reasonable schedule to correct the deficiency, and have written

justification for continued operation which will be available for

NRC review. In addition:

for inoperable equipment not covered by

the plant technical specifications, the licensee may continue

reactor operation if the safety function carn be accomplished by

8

other designated equipment that is qualified, or if limited

administrative controls can be used to ensure the safety function is

performed.

Based on the information reviewed, as discussed above, the inspector

considered that the licensee's NCR arid 10 CFR 50.59 evaluation did not

provide an adequate assessment or documentation in accordance with

10 CFR 50.49 requirements. In particular, the 10 CFR 50.59 evaluation

credited alternate instrumentation for accomplishing the safety

function despite the fact that none of the listed variables provides

real time core reactivity information and no administrative controls

were established (e.g., control room operators-were not notified of

the potential for these monitors to fail during post accident conditions).

This is considered a violation of NRC requirements (50-361/89-11-01).

The inspector discussed concerns with the safety evaluation for

NCR G-0865 Revision 0, with the site QA groups. In particular, the

inspector was concerned that a sufficiently critical review of the

NCR was not made (in 1988) since the disposition of the NCR was approved

by QA. The QA Manager acknowledged the inspector's concerns and

indicated that the present QA organization has been sensitized to

the need for critical reviews .of such things as NCRs.

In addition, the

inspector was informed that Edison was evaluating the need for the

independent safety engineering group (ISEG) to review the disposition

of NCRs for technical adequacy. The inspector will review the

licensee's actions on this matter which is identified as followup

item (50-361/89-11-02).

The inspector's concerns over this matter were discussed durina an

exit meeting conducted on March 17, 1989. During that meetina, SCE

committed to revising the NCR and providing a justification for

continued operation (JCO) to the NRC by March 24, 1989.

NCR G-0865, Revision 1, was sent to the NRC on March 23, 1989.

The

NCR was reviewed by the inspector and considered to be inadequate.

In particular, the inspector had the following concerns with the

revised NCR:

-

The safety evaluation and JCO relied on the same Technical

Specification instrumentation/parameters for accident

monitoring that were indicated in the original NCR.

The final disposition of the revised NCR identified that the

unqualified connectors would be repaired or replaced as

necessary prior to return to service from the Cycle 5 refueling

outage.

Due to the potential significance of this issue the inspector

conducted a followup inspection on this matter on April 3 through

April 7, 1989.

The inspector continued discussions with the

licensee in attempt to resolve this matter.

During the followup inspection the inspector identified additional

concerns:

9

The inspector reviewed the Unit 2/3 Updated Final Safety

Analysis Report (UFSAR). During that review, the inspector

noted that Table 3.11.5 and Table 7.5-2 list the post accident

monitoring instrumentation (PAMI) used in the Units.

However,

the excore neutron monitors were not listed.

A tour of the Unit 2/3 control rooms revealed that PAMI meters

are stenciled as such on the control panels. However, the

startup log power excore neutron monitors were not designated

as PAMI.

Discussions with reactor operators (ROs), senior reactor

operators (SROs), and the Unit 2/3 Superintendent revealed that

they had not been notified of the problems with the connectors

for the excore neutron monitors and that they could not be

relied upon during a DBA. In addition, the inspector also

found that the ROs and SROs were not aware that the excore

neutron monitors were PAMI.

The inspector discussed these concerns with the licensee who were

evaluating the reasons for these discrepancies.

They will be

reviewed during a future inspection as unresolved item

(50-361/89-11-03).

On April 6, 1989, the inspector continued discussions with Edison

personnel over the unqualified connectors. During this meeting, the

license indicated that they had contacted the vendor for more

detailed information concerning the failures. The results of the

discussions were that the vendor had informed Edison that all of the

connectors sent by licensees had been tested and had failed.

However, the failures were in a conservative direction (higher

indicated counts than actual) and tended to be time dependent. The

time dependency was largely contingent upon the extent of the

oricinal flaw.

The inspector discussed the concern over use of alternate monitoring

means with the licensee who stated that this instrumentation was

credited for post accident monitoring during the original safety

analysis. The inspector acknowledged this, but indicated that

Edison had committed to Regulatory Guide 1.97 since the original

safety analysis and .that the Regulatory Guide specified the excore

neutron monitors as the primary core reactivity monitoring

instrumentation. With regards to completing repairs to the

connectors during the next refueling outage, the inspector pointed

out that the next refueling outage for Unit 3 is scheduled for fall

1990 and that the licensee would not be able to determine core

reactivity (real time) if a DBA should occur.

These concerns were discussed in the followup exit meeting of April

10, 1989.

During that meeting, SCE representatives committed to

perform a reevaluation of the ability of other designated equipment

to accomplish the post-accident safety function of monitoring core

reactivity and to revise the NCR to provide for repair or replacement of

the unqualified connectors during the next outage of sufficient duration

10

after receiving a qualified unit from the vendor. Revision 2 of the

NCR and JCO were reviewed by the NRC on April 14, 1989. The licensee

indicated that compensatory actions would be established for the

operators to evaluate questionable readings from the excore neutron

monitors and borate the reactor unless a sufficient shutdown margin

could be demonstrated. In addition, the licensee committed to

inspect, test and repair, or replace the connectors during the next

outage of sufficient duration (no later than the completion of the Cycle

5 refueling outage).

The inspector considered that the evaluations in

Revision 2 of the NCR and JCO were acceptable. Also, the licensee

was aggressively pursuing correcitve actions with the vendor.

b. .(Closed) Unresolved Item (206/87-02-02), "Identification Of

Unqualified AMP Butt Splices"

This item identified a concern raised during an NRR Vendor Program

Branch inspection in February and March 1987. The concern related

to the question of whether AMP butt splices were actually used in

harsh environments.

This item was readdressed in inspection report

50-206/88-17. At that time the inspector also raised questions as

to the operability conclusion of the non-qualified splices found

and whether inspection of additional splices was necessary.

The inspector reviewed the status of this item and noted that the

licensee evaluated this condition and reported conditions found in

licensee event report (LER) 87-06, Revision 1. In this LER, Edison

indicated that a walkdown was performed to determine if there were

any unqualified splices.

During this review, the licensee noted

that the splices for both trains of the containment wide range water

level instrumentation were unqualified. The licensee subsequently

repaired the unqualified splices.

The root cause of the condition

was attributed to an erroneous deletion of termination details

on a revision of a drawing note associated with those particular

terminations. The licensee identified that they inspected

approximately 60% of the butt splices located inside the Unit 1

containment. Of those, four splices were found to be unqualified.

Since the unqualified splices could be attributed to a unique cause,

the inspector considered that the licensee's actions were

appropriate. This item is closed.

C.

(Closed) Followup Item (206/87-20-01), "Followup Of IIT Items

For Cycle 9 Refueling Outage"

This item identified a number of cycle 9 outage items that had not

been completed that were being tracked to completion. The inspector

reviewed the remaining items on the list and discussed their status

with licensee personnel. The results of this review are as follows:

(1) Electrical cable monitoring program - The licensee purchased a

system to analyze cables and a program was established and

proceduralized (Procedure SO1 XXVII-30, "Cable and Electrical

Apparatus Monitoring Program").

Discussions with the licensee

revealed that they had tested approximately 500 circuits which

roughly corresponded to approximately 1600 cables. Cables were

11

selected based on maintenance records or if their adequacy was.

questionable. The results from these tests were being

evaluated.

(2) Third auxiliary feedwater pump procedures - The licensee

indicated that the emergency operating instructions were

completed and in the review process.

Regular operating

instructions were being prepared at this time to include the

new system design. Completion of the revised operating

procedures will be performed by the next refueling. The NRC

was reviewing the new EOI guidelines for approval.

(3) Nitrogen backup for main feedwater regulating valve - The

licensee issued design change package (DCP) 3472 to install the

backup nitrogen. This was implemented during the Cycle .X

outage.

(4) Check valve wear test -

The licensee performed an assessment of

the accelerated check valve wear test results and concluded

that continuous operation will result in wear exceeding

manufacturers recommendations with one to two additional cycles

of power operation. As a result, the assessment recommended

procurement of modified replacement discs.

The licensee was

evaluating the recommendations from this review.

The inspector considered that the licensee's actions (and proposed

actions) on these items were appropriate. Therefore, this followup

item is closed.

d.

(Closed) Part 21 Report (50-206/88-06-P), "Defective Replated Clevite

Bearings Used In General Motors Diesel Generators"

This Part 21 report identified a defect in Clevite upper connecting

rod bearings used in the emergency diesel generators manufactured by

General Motors Electro Motive Division.

This item is not applicable to Unit 1 since Transamerica Delaval

Inc. diesel generators are used and the licensee did not install any

Clevite bearings in the Unit 1 D/G. This item was closed for Units

2 and 3 in inspection report 50-361/88-28; 50-362/88-27.

e.

(Closed) Followup Item (206/88-02-01), "Annual 50.59 Report

Review For All Units"

This item concerned the fact that the licensee's annual facility

modification evaluation report dealt mainly with modifications that

had been funded rather than completed. The concern was, if the

decision was made later to not install the modification, how would

this be handled.by the licensee and what effect did it have on

subsequent submittals (i.e., Safety Analysis Report updates).

The inspector discussed this concern with Edison personnel who

indicated that the annual report was not used by SCE other to inform

the NRC of intended modifications. Since it was not used to track

12

the status of these modifications or used for updating the Safety

Analysis Report, the licensee did not consider that it would be

confusing to them should a modification not be installed. They also

considered that, if a proposed modification were altered during

installation, it would be identified to the NRC during the next

annual update. Based upon this conversation, the inspector

considered reporting changes in this manner was satisfactory. This

item is closed.

f.

(Closed) Followup Item (206/87-12-01), "Followup On Licensee's

Justification For Amount Of Time To Implement A Design Change"

This item identified a concern with regard to theamount of time to

implement a design change for the containment spray low flow

annunciator. In particular, the design change was prepared in 1979,

but had not been implemented for 9 years.

The inspector discussed this concern with the licensee and learned

that most of the work to install a containment spray low flow

annunciator had been completed during this outage. The balance of

the work was considered to be workable with the plant on-line

and is currently planned for completion after return to service.

The licensee indicated that the long period of time to implement the

design change-was a result of a transfer in methodology for making

design changes that occurred in 1979. Edison indicated that in the

old process they could not tell what had been implemented and what

hac not.

The current program requires that the drawings be revised

when the work is completed. In addition, the DCP process requires

as-built verification of the elementary drawings. The licensee

indicated that they were not aware of any other problems such as

this. However, walkdowns of the P&IDs to compare with as-built

conditions was in process as part of another program. The inspector

considered that the licensee's actions were appropriate and that the

as-built verification process should be adequate to find additional

discrepancies. Therefore, this item is closed.

g.

(Closed) (206/TI-15-91), "Licensee's Actions In Accordance With

Generic Letter 83-18"

This inspector reviewed the licensee's modifications to the reactor

trip breakers per the requirements of Temporary Instruction 2515/91

and documented the results in inspection report 50-206/88-12;

50-361/88-09; and 50-362/88-09. In that report, the inspector

identified that this issue was closed for Units 2 and 3, but it

would remain open for Unit 1 since there were no provisions for

on-line testing of the Unit 1 Reactor Trip breakers inspectors.

Since that inspection, this item was resolved in a letter to the

licensee dated September 16, 1988 in which NRR agreed that on-line

testing of these breakers was not required. Therefore, this item is

closed.

One violation was identified in Paragraph 4.a.

13

5. Exit Meeting

(30703)

On March 17, and on April 7, 1989, exit meetings were held with the

licensee representatives identified in paragraph 1. The inspector

summarized the inspection scope and findings as described in this report.

During these meetings, SCE representatives acknowledged the violation

identified in Paragraph 4.a. In addition, the licensee committed to

performing a reevaluation of the operability of the excore neutron

-monitors and providing justifications for continued operation for NRC

review as discussed in Paragraph 4.a. These commitments were

satisfactorily met by the licensee.

The licensee did not identify as proprietary any of the materials

reviewed or discussed during this inspection.