Letter Sequence Other |
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Results
Other: LIC-03-0164, Response to a RAI on Measurement Uncertainty Recapture Power Uprate, LIC-04-0006, Closure of NRC Tack Issues for Fort Calhoun Station Unit No. 1, LIC-04-0061, Notification of Technical Issues Associated with License Amendment No. 225, ML032870394, ML040210313, ML040400333, ML040490383, ML041060362, ML041310501, ML041390246, ML042120203, ML043350135, ML043370117, ML050530011, ML050600428, ML050610222, ML050750059
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MONTHYEARLIC-03-0067, Amendment Request for License DPR-40 Measurement Uncertainty Recapture Power Uprate2003-07-18018 July 2003 Amendment Request for License DPR-40 Measurement Uncertainty Recapture Power Uprate Project stage: Request 05000285/LER-2003-002, Regarding Inadequate Testing of Diesel Generators Due to Air Start Systems Unique Design2003-08-28028 August 2003 Regarding Inadequate Testing of Diesel Generators Due to Air Start Systems Unique Design Project stage: Request ML0324505182003-08-28028 August 2003 Revision of License Amendment Request, Measurement Uncertainly Recapture Power Uprate Project stage: Request LIC-03-0142, Completion of Recirculation Actuation Logic Channel Functional Test Circuitry Modification2003-10-14014 October 2003 Completion of Recirculation Actuation Logic Channel Functional Test Circuitry Modification Project stage: Request ML0328705202003-10-14014 October 2003 RAI, Measurement Uncertainty Recapture Power Uprate Project stage: RAI ML0328703942003-10-14014 October 2003 Withholding from Public Disclosure, Calculation Number FC-6896-P, Secondary Calorimetric Uncertainty Analysis Project stage: Other LIC-03-0148, Response to Request for Additional Information - Measurement Uncertainty Recapture Power Uprate2003-10-31031 October 2003 Response to Request for Additional Information - Measurement Uncertainty Recapture Power Uprate Project stage: Response to RAI LIC-03-0077, License Amendment Request, Addition of Diesel Generator Fuel Oil, Diesel Generating Lubrication Oil, and Diesel Generator Starting Air Requirements2003-12-0101 December 2003 License Amendment Request, Addition of Diesel Generator Fuel Oil, Diesel Generating Lubrication Oil, and Diesel Generator Starting Air Requirements Project stage: Request LIC-03-0159, November 2003 Monthly Operating Report for Fort Calhoun Unit 12003-12-15015 December 2003 November 2003 Monthly Operating Report for Fort Calhoun Unit 1 Project stage: Request LIC-03-0164, Response to a RAI on Measurement Uncertainty Recapture Power Uprate2003-12-15015 December 2003 Response to a RAI on Measurement Uncertainty Recapture Power Uprate Project stage: Other LIC-03-0166, Response to Request for Additional Information Regarding Measurement Uncertainty Recapture Power Uprate2003-12-22022 December 2003 Response to Request for Additional Information Regarding Measurement Uncertainty Recapture Power Uprate Project stage: Response to RAI ML0402007572004-01-16016 January 2004 Issuance of License Amendment 224 Revising the Renewed Operating License and the TSs to Increase the Licensed Rated Power by 1.6 Percent from 1500 Megawatts Thermal (Mwt) to 1524 Mwt Project stage: Approval ML0402103132004-01-16016 January 2004 Tech Spec Pages for Amendment 224 Revising the Renewed Operating License and the TSs to Increase the Licensed Rated Power by 1.6 Percent from 1500 Megawatts Thermal (Mwt) to 1524 Mwt Project stage: Other LIC-04-0015, Response to RAI Regarding Fort Calhoun, Unit 1, License Amendment Request, Various Administrative and Editorial Changes2004-02-0909 February 2004 Response to RAI Regarding Fort Calhoun, Unit 1, License Amendment Request, Various Administrative and Editorial Changes Project stage: Response to RAI ML0404003332004-02-0909 February 2004 Public Notice of Application for Amendment to Facility Operating License Project stage: Other ML0404903832004-02-13013 February 2004 Amendment, Changes Implementation Date from 30 Days to 120 Days for Amendment No. 224 Issued on 01/16/2004 That Approved Measurement Uncertainty Uprate to Increase Licensed Rated Power by 1.6 Percent from 1500 Megawatts Thermal to 1524 Project stage: Other ML0405803462004-02-18018 February 2004 RAI, License Amendment Request Administrative TS Changes (Tac. MC1535) Project stage: RAI ML0410603622004-04-14014 April 2004 Memo to File, E-mail Regarding Fort Calhoun Emergency Diesel Generating Starting Air System Project stage: Other LIC-04-0061, Notification of Technical Issues Associated with License Amendment No. 2252004-05-0505 May 2004 Notification of Technical Issues Associated with License Amendment No. 225 Project stage: Other ML0413105012004-05-10010 May 2004 5/10/04, Fort Calhoun, Unit 1 - Public Notice of Application for Amendment to Facility Operating License Project stage: Other ML0413902462004-05-14014 May 2004 License Amendment, Amendment Restores Licensed Thermal Power from 1524 Mega Thermal Project stage: Other ML0413901262004-05-14014 May 2004 5/14/04, Fort Calhoun, Unit 1 - TS - Issuance of Amendment Project stage: Approval LIC-04-0073, Response to Request for Additional Information Regarding License Amendment Request, Addition of Diesel Generator Fuel Oil, Diesel Generator Lubricating Oil, & Diesel Generator Starting Air Requirements2004-07-0202 July 2004 Response to Request for Additional Information Regarding License Amendment Request, Addition of Diesel Generator Fuel Oil, Diesel Generator Lubricating Oil, & Diesel Generator Starting Air Requirements Project stage: Response to RAI ML0421202032004-07-23023 July 2004 Tech Spec Pages for Amendment 228 Various Administrative and Editorial Changes Project stage: Other ML0421104112004-07-23023 July 2004 Issuance of License Amendment 228 Various Administrative and Editorial Changes Project stage: Approval ML0424300272004-08-27027 August 2004 RAI, Modify Technical Specification 2.3.(4) Project stage: RAI LIC-04-0094, Supplemental Response to the Requests for Additional Information on the Fort Calhoun, Unit 1 Security Plan and Safeguards Contingency Plan2004-08-27027 August 2004 Supplemental Response to the Requests for Additional Information on the Fort Calhoun, Unit 1 Security Plan and Safeguards Contingency Plan Project stage: Supplement ML0433501352004-10-21021 October 2004 Tech Spec Pages for Amendment No. 229, Changing TS 2.7, TS Table 3-5 and TS 5.0 to Modify Requirements for the Diesel Generator Fuel Oil for Consistency with Improved Standard TS Project stage: Other ML0430205742004-10-21021 October 2004 Issuance of License Amendment No. 229, Changing TS 2.7, TS Table 3-5 and TS 5.0 to Modify Requirements for the Diesel Generator Fuel Oil for Consistency with Improved Standard TS Project stage: Approval LIC-04-0102, Request for Additional Information (RAI) Regarding License Amendment Request (Lar), Trisodium Phosphate (TSP) Dodecahydrate Volume2004-10-29029 October 2004 Request for Additional Information (RAI) Regarding License Amendment Request (Lar), Trisodium Phosphate (TSP) Dodecahydrate Volume Project stage: Request ML0433701172004-11-0808 November 2004 TS Pages for Amendment No. 230 Relocating Requirements of TS 3.3(1)a and Other Components Subject to ASME XI Boiler & Pressure Vessel Code Inspection and Testing Surveillance and TS 3.4 to Update UFSAR Project stage: Other ML0432705302004-11-0808 November 2004 Issuance of License Amendment No. 230 Relocating Requirements of TS 3.3(1)a and Other Components Subject to ASME XI Boiler & Pressure Vessel Code Inspection and Testing Surveillance and TS 3.4 to Update UFSAR Project stage: Approval LIC-04-0133, Response to NRC RAI on Trisodium Phosphate (TSP) License Amendment Request2004-12-16016 December 2004 Response to NRC RAI on Trisodium Phosphate (TSP) License Amendment Request Project stage: Response to RAI ML0505300112005-02-18018 February 2005 Tech Spec Page for Amendment 231 Elimination of Requirements to Provide Monthly Operating/Annual Occupational Radiation Exposure Reports Project stage: Other ML0505500612005-02-18018 February 2005 Issuance of License Amendment 231 Elimination of Requirements to Provide Monthly Operating/Annual Occupational Radiation Exposure Reports Project stage: Approval ML0506004282005-03-0101 March 2005 Amendment, Revision of TS Section 2.3(4) & TS Section 3.6(2)d.(i) Project stage: Other ML0506102222005-03-0101 March 2005 Technical Specifications, Revision of TS Section 2.3(4) & TS Section 3.6(2)d.(i) Project stage: Other ML0507500592005-03-11011 March 2005 Tech Spec Pages for Amendment 233 Revising TS 5.9.5 to Be Consistent with Specification 5.6.5 of NUREG-1432 Project stage: Other ML0507505342005-03-11011 March 2005 Issuance of License Amendment 233 Revising TS 5.9.5 to Be Consistent with Specification 5.6.5 of NUREG-1432 Project stage: Approval LIC-04-0006, Closure of NRC Tack Issues for Fort Calhoun Station Unit No. 12005-07-0101 July 2005 Closure of NRC Tack Issues for Fort Calhoun Station Unit No. 1 Project stage: Other 2004-02-13
[Table View] |
Tech Spec Pages for Amendment 224 Revising the Renewed Operating License and the TSs to Increase the Licensed Rated Power by 1.6 Percent from 1500 Megawatts Thermal (Mwt) to 1524 Mwt| ML040210313 |
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Fort Calhoun  |
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| Issue date: |
01/16/2004 |
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NRC/NRR/DLPM/LPD4 |
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| ML040200777 |
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| TAC MC0029 |
| Download: ML040210313 (3) |
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Text
TECHNICAL SPECIFICATIONS DEFINITIONS The following terms are defined for uniform interpretation of these Specifications.
REACTOR OPERATING CONDITIONS Rated Power A steady state reactor core output of 1524 MWt.
Reactor Critical The reactor is considered critical for purposes of administrative control when the neutron flux logarithmic range channel instrumentation indicates greater than 104 % of rated power.
Power Operation Condition (Operating Mode 1)
The reactor is in the power operation condition when it is critical and the neutron flux power range instrumentation indicates greater than 2% of rated power.
Hot Standby Condition (Operating Mode 2)
The reactor is considered to be in a hot standby condition if the average temperature of the reactor coolant (Tavg) is greater than 5151F, the reactor is critical, and the neutron flux power range instrumentation indicates less than 2% of rated power.
Hot Shutdown Condition (Operating Mode 3)
The reactor is in a hot shutdown condition if the average temperature of the reactor coolant (Tavg) is greater than 5150F and the reactor is subcritical by at least the amount defined in Paragraph 2.10.2.
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Amendment No. 63,50,224
2.0 LIMITING CONDITIONS FOR OPERATION 2.1 Reactor Coolant System (continued) 2.1.6 Pressurizer and Main Steam Safety Valves (continued)
Action statements (5)b. and c. include the removal of power from a closed block valve to preclude any inadvertent opening of the block valve at a time the PORV may not be closed due to maintenance.
However, the applicability requirements of the LCO to operate with the block valve(s) closed with power maintained to the block valve(s) are only intended to permit operation of the plant for a limited period of time not to exceed the next refueling shutdown (Mode 5), so that maintenance can be performed on the PORV(s) to eliminate the seat leakage condition.
To determine the maximum steam flow, the only other pressure relieving system assumed operational is the main steam safety valves. Conservative values for all systems parameters, delay times and core moderator coefficients are assumed. Overpressure protection is provided to portions of the reactor coolant system which are at the highest pressure considering pump head, flow pressure drops and elevation heads.
If no residual heat were removed by any of the means available, the amount of steam which could be generated at safety valve lift pressure would be less than half of the capacity of one safety valve. This specification, therefore, provides adequate defense against overpressurization when the reactor is subcritical.
Performance of certain calibration and maintenance procedures on safety valves requires removal from the pressurizer. Should a safety valve be removed, either operability of the other safety valve or maintenance of at least one nozzle open to atmosphere will assure that sufficient relief capacity is available. Use of plastic or other similar material to prevent the entry of foreign material into the open nozzle will not be construed to violate the "open to atmosphere" provision, since the presence of this material would not significantly restrict the discharge of reactor coolant.
The total relief capacity of the ten main steam safety valves is 6.606 x 1 O6 lb/hr. If, following testing, the as found setpoints are outside +/-1% of nominal nameplate values, the valves are set to within the +1-1%
tolerance. The main steam safety valves were analyzed for a total loss of main feedwater flow while operating at RATED POWER(3) to ensure that the peak secondary pressure was less than 1100 psia, the ASME Section III upset pressure limit of 10% greater than the design pressure. At RATED POWER, sufficient relief valve capacity is available to prevent overpressurization of the steam system on loss-of-load conditions.(4) These analyses are based on a minimum of four-of-five operable main steam safety valves on each main steam header.
The power-operated relief valve low setpoint will be adjusted to provide sufficient margin, when used in conjunction with Technical Specification Sections 2.1.1 and 2.3, to prevent the design basis pressure transients from causing an overpressurization incident. Limitation of this requirement to scheduled cooldown ensures that, should emergency conditions dictate rapid cooldown of the reactor coolant system, inoperability of the low temperature overpressure protection system would not prove to be an inhibiting factor. The effective full flow area of an open PORV is 0.94 in2.
Removal of the reactor vessel head provides sufficient expansion volume to limit any of the design basis pressure transients. Thus, no additional relief capacity is required.
References (1) Article 9 of the 1968 ASME Boiler and Pressure Vessel Code,Section III (2) USAR, Section 14.9 (3) USAR, Section 14.10 (4) USAR, Sections 4.3.4, 4.3.9.5 2-16 Amendment No. 39,47,54,146,161,189,224
3.0 SURVEILLANCE REQUIREMENTS 3.0 SURVEILLANCE REQUIREMENTS 3.5 Containment Tests (Continued)
Basis The containment is designed for an accident pressure of 60 psig.(2) While the reactor is operating, the internal environment of the containment will be air at approximately atmospheric pressure and a maximum temperature of about 120'F. With these initial conditions the temperature of the steam-air mixture at the peak accident pressure of 60 psig is 2880F.
Prior to initial operation, the containment was strength-tested at 69 psig and then was leak tested. The design objective of the pre-operational leakage rate test has been established as 0.1% by weight for 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> at 60 psig. This leakage rate is consistent with the construction of the containment, which is equipped with independent leak-testable penetrations and contains channels over all inaccessible containment liner welds, which were independently leak-tested during construction.
Safety analyses have been performed on the basis of a leakage rate of 0.1% of the free volume per day of the first 24 hours2.777778e-4 days <br />0.00667 hours <br />3.968254e-5 weeks <br />9.132e-6 months <br /> following the maximum hypothetical accident. With this leakage rate, at RATED POWER, and with minimum containment engineered safety systems for iodine removal in operation (one air cooling and filtering unit), the public exposure would be well below 10 CFR Part 100 values in the event of the maximum hypothetical accident.(3) The performance of an integrated leakage rate test and performance of local leak rate testing of individual penetrations at periodic intervals during plant life provides a current assessment of potential leakage from the containment.
The reduced pressure (5 psig) test on the PAL is a conservative method of testing and provides adequate indication of any potential containment leakage path. The test is conducted by pressurizing between two resilient seals on each door. The test pressure tends to unseat the resilient seals which is opposite to the accident pressure that tends to seat the resilient seals. A periodic test ensures the overall PAL integrity at 60 psig.
The integrated leakage rate test (Type A test) can only be performed during refueling shutdowns.
3-51 Amendment No. 68,97,139,151,185,216,224