ML032900004

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IR 05000325-03-005, 05000324-03-005, on 06/22/2003 - 09/20/2003; Brunswick Steam Electric Plant, Units 1 and 2; Problem Identification and Resolution. Non-Cited Violation Noted
ML032900004
Person / Time
Site: Brunswick  Duke Energy icon.png
Issue date: 10/16/2003
From: Fredrickson P
NRC/RGN-II/DRP/RPB4
To: Keenan J
Carolina Power & Light Co
References
IR-03-005
Download: ML032900004 (23)


See also: IR 05000324/2003005

Text

October 16, 2003

Carolina Power and Light Company

ATTN: Mr. J. S. Keenan

Vice President

Brunswick Steam Electric Plant

P. O. Box 10429

Southport, NC 28461

SUBJECT: BRUNSWICK STEAM ELECTRIC PLANT - NRC INTEGRATED INSPECTION

REPORT NOS. 05000325/2003005 AND 05000324/2003005

Dear Mr. Keenan:

On September 20, 2003, the Nuclear Regulatory Commission (NRC) completed an inspection

at your Brunswick Units 1 and 2 facilities. The enclosed integrated inspection report documents

the inspection findings, which were discussed on September 17, 2003, with you and other

members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

The report documents one NRC-identified finding of very low safety significance (Green). This

finding was determined to involve a violation of NRC requirements. However, because of the

very low safety significance and because it is entered into your corrective action program, the

NRC is treating this finding as a non-cited violation (NCV) consistent with Section VI.A of the

NRC Enforcement Policy. If you contest the non-cited violation, you should provide a response

within 30 days of the date of this inspection report, with the basis for your denial, to the Nuclear

Regulatory Commission, ATTN.: Document Control Desk, Washington, DC 20555-0001; with

copies to the Regional Administrator Region II; the Director, Office of Enforcement, United

States Nuclear Regulatory Commission, Washington, DC 20555-0001; and the NRC Resident

Inspector at the Brunswick Steam Electric Plant.

CP&L 2

In accordance with 10CFR 2.790 of the NRCs Rules of Practice, a copy of this letter and its

enclosure will be available electronically for public inspection in the NRC Public Document

Room or from the Publicly Available Records (PARS) component of NRCs document system

(ADAMS). ADAMS is accessible from the NRC Web site at http://www.nrc.gov/reading-

rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

Paul E. Fredrickson, Chief

Reactor Projects Branch 4

Division of Reactor Projects

Docket Nos.: 50-325, 50-324

License Nos: DPR-71, DPR-62

Enclosure: Inspection Report 05000325, 324/2003005

w/Attachment: Supplemental Information

cc w/encl: (See page 3)

CP&L 3

cc w/encl:

C. J. Gannon, Director Peggy Force

Site Operations Assistant Attorney General

Brunswick Steam Electric Plant State of North Carolina

Carolina Power & Light Electronic Mail Distribution

Electronic Mail Distribution

Robert P. Gruber

W. C. Noll Executive Director

Plant Manager Public Staff NCUC

Brunswick Steam Electric Plant 4326 Mail Service Center

Carolina Power & Light Company Raleigh, NC 27699-4326

Electronic Mail Distribution

Public Service Commission

James W. Holt, Manager State of South Carolina

Performance Evaluation and P. O. Box 11649

Regulatory Affairs CPB 7 Columbia, SC 29211

Carolina Power & Light Company

Electronic Mail Distribution David R. Sandifer, Chairperson

Brunswick County Board of

Edward T. ONeil, Manager Commissioners

Site Support Services P. O. Box 249

Carolina Power & Light Company Bolivia, NC 28422

Brunswick Steam Electric Plant

Electronic Mail Distribution Dan E. Summers

Emergency Management Coordinator

New Hanover County Department of

Leonard Beller, Supervisor Emergency Management

Licensing/Regulatory Programs P. O. Box 1525

Carolina Power and Light Company Wilmington, NC 28402

Electronic Mail Distribution

Steven R. Carr

Associate General Counsel - Legal Dept.

Progressive Energy Service Company, LLC

P.O. Box 1551

Raleigh, North Carolina 27602-1551

John H. ONeill, Jr.

Shaw, Pittman, Potts & Trowbridge

2300 N. Street, NW

Washington, DC 20037-1128

Beverly Hall, Acting Director

Division of Radiation Protection

N. C. Department of Environment

and Natural Resources

Electronic Mail Distribution

CP&L

B. Mozafari, NRR

L. Slack, RII EICS

RIDSNRRDIPMLIPB

PUBLIC

OFFICE DRP/RII DRP/RII DRP/RII DRP/RII

SIGNATURE GTM JDA JAC6 EMD

NAME GMacdonald:as JAustin JCanady EDiPaolo

DATE 10/16/2003 10/16/2003 10/16/2003 10/16/2003

E-MAIL COPY? YES NO YES NO YES NO

PUBLIC DOCUMENT YES NO

OFFICIAL RECORD COPY DOCUMENT NAME: C:\ORPCheckout\FileNET\ML032900004.wpd

U. S. NUCLEAR REGULATORY COMMISSION

REGION II

Docket Nos: 50-325, 50-324

License Nos: DPR-71, DPR-62

Report Nos: 05000325/2003005 and 05000324/2003005

Licensee: Carolina Power and Light

Facility: Brunswick Steam Electric Plant, Units 1 & 2

Location: 8470 River Road SE

Southport, NC 28461

Dates: June 22, 2003 - September 20, 2003

Inspectors: E. DiPaolo, Senior Resident Inspector

J. Canady, Acting Senior Resident Inspector

J. Austin, Resident Inspector

Approved by: Paul Fredrickson, Chief,

Reactor Projects Branch 4

Division of Reactor Projects

Enclosure

SUMMARY OF FINDINGS

IR 05000325/2003-005, 05000324/2003-005; 06/22/2003 - 09/20/2003; Brunswick Steam

Electric Plant, Units 1 and 2; Problem Identification and Resolution.

The report covered a three-month period of inspection by resident inspectors. One Green non-

cited violation (NCV) was identified. The significance of most findings is indicated by its color

(Green, White, Yellow, Red) using Inspection Manual Chapter (IMC) 609, Significance

Determination Process (SDP). Findings for which the SDP does not apply may be Green or be

assigned a severity level after NRC management review. The NRC's program for overseeing

the safe operation of commercial nuclear power reactors is described in NUREG-1649,

Reactor Oversight Process, Revision 3, dated July 2000.

A. NRC-Identified and Self-Revealing Findings

Cornerstone: Initiating Events and Mitigating Systems

Green. The inspectors identified a non-cited violation for the licensees failure to comply

with 10 CFR 50, Appendix B, Criterion XVI. This violation is related to inadequate

corrective actions to prevent recurring nuclear and conventional service water pump

functional failures caused by clogging of the associated pumps strainer due to marine

growth in the service water intake bays. This resulted in six failures in twelve months.

This finding is greater than minor because it resulted in an increase in the likelihood of

loss of nuclear and conventional service water initiating events. In addition, the finding

affected the operability, availability, and reliability of the nuclear and conventional

service water pumps. The finding is of very low safety significance because redundancy

existed in the nuclear and conventional service water systems and the relatively short

duration of unavailability of the pumps. (Section 4OA2)

B. Licensee Identified Violations

None.

REPORT DETAILS

Summary of Plant Status

Unit 1 began the report period operating at full power. On July 1, 2003, the unit was shutdown

for a forced outage due to drywell unidentified leakage exceeding Technical Specification (TS)

requirements. The Unit was returned to full power on July 6, following drywell leakage repairs.

On July 11, reactor power was reduced to 70% power to facilitate repairs of a steam leak on the

B feedwater heater string. Full power was reached the following day, and the Unit remained at

approximately full power for the remainder of the inspection period.

Unit 2 began the report period operating at full power. Power was reduced to approximately

50% on August 22 for a rod sequence exchange, various planned corrective and preventive

maintenance activities, and surveillance testing. Power was returned to full power on

August 25, and the Unit remained at approximately full power for the remainder of the

inspection period.

1. REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity

1R01 Adverse Weather Protection

a. Inspection Scope

The inspectors reviewed the licensees preparations for severe weather conditions

during hurricane season. The inspectors toured protected area and exterior plant

grounds for loose debris which could pose hazards to plant equipment during high

winds, and reviewed preparations for increased accumulation of rain water. The

inspectors selected risk-significant and susceptible systems and areas for review.

These included the electrical switch yard, the hydrogen tank storage area, the

radioactive waste building, the emergency diesel generator building and the service

water structure.

During the approach of Hurricane Isabel to the Cape Fear Region of North Carolina, the

inspectors attended hurricane preparation status meetings and reviewed provisions for

relief of plant operators, security guards, and emergency response organization

personnel. Licensee preparations for plant damage assessment were also reviewed.

On September 17 and 18, 2003, the inspectors observed the licensees emergency

response facility staffs monitoring of storm conditions, damage assessment and

corrective actions.

During these inspections, the following procedures were reviewed to verify that the

licensees actions were consistent with severe weather program requirements:

  • Plant Emergency Procedure 0PEP-02.6, Severe Weather
  • Administrative Instruction 0AI-68, Brunswick Nuclear Plant Response to Severe

Weather Warning

  • Abnormal Operating Procedure 0AOP-13.0, Operation During Hurricane, Flood

Conditions, Tornado, or Earthquake

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b. Findings

No findings of significance were identified.

1R04 Equipment Alignment

a. Inspection Scope

The inspectors performed three partial walkdowns of the below listed systems to verify

that the systems were correctly aligned while the redundant train or system was

inoperable or out-of-service (OOS) or, for single train risk significant systems, while the

system was available in a standby condition. The inspectors assessed conditions such

as equipment alignment (i.e., valve positions, damper positions, and breaker alignment)

and system operational readiness (i.e., control power and permissive status) that could

affect operability. The inspectors verified that the licensee identified and resolved

equipment alignment problems that could cause initiating events or impact mitigating

system availability. Administrative procedure ADM-NGGC-0106, Configuration

Management Program Implementation, was reviewed by the inspectors to verify that

available structure, system or components (SSCs) met the requirements of the

licensees configuration control program.

number 3 OOS due to maintenance)

In determining correct system lineup, the inspectors reviewed Procedure OPT-12.8.1,

Breaker Alignment Operability Test, 2OP-18, Core Spray System Operating Procedure,

and 1OP-16, Reactor Core Isolation Cooling (RCIC) System Operating Procedure.

b. Findings

No findings of significance were identified.

1R05 Fire Protection

1. Fire Area Walkdowns

a. Inspection Scope

The inspectors reviewed current action requests (ARs) and work orders (WOs)

associated with the fire suppression system to confirm that their disposition was in

accordance with OAP-033, Fire Protection Program Manual. The inspectors reviewed

the status of ongoing surveillance activities to verify that they were current to support the

operability of the fire protection system. In addition, the inspectors observed the fire

suppression and detection equipment to determine whether any conditions or

deficiencies existed which would impair the operability of that equipment. The

inspectors toured the following areas important to reactor safety and reviewed the

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associated Prefire Plans to verify that the requirements for fire protection design

features, fire area boundaries, and combustible loading were met:

and the north and south residual heat removal (RHR) rooms, Prefire Plan

1PFP-RB, Reactor Building Prefire Plans (three areas)

  • Unit 1 reactor building, nine and 20 foot elevations, north and south RHR heat

exchanger rooms, Prefire Plan 1PFP-RB, Reactor Building Prefire

Plans (2 areas)

  • Diesel generator building number two cell, 23-foot elevation. Prefire plan

OPFP-DG Diesel Generator Building Prefire Plans

  • Units 1 and 2 reactor building, 23-foot elevation, battery rooms 1A, 1B, 2A, and

2B, Prefire Plan 0PFP-CB, Control Building Prefire Plans (four areas)

To assess the licensees ability to identify and correct adverse conditions, the inspectors

reviewed the licensees actions in response to AR 102494102494which identified incorrect test

requirements for the station emergency lighting unit batteries.

b. Findings

No findings of significance were identified.

2. Fire Drill

a. Inspection Scope

On September 5, 2003, the inspectors observed an unannounced plant fire drill in the

Unit 2 reactor building, to assess the fire brigade performance and to verify that proper

firefighting techniques for the type of fire encountered were utilized. The inspectors

monitored the fire brigades use of protective equipment and firefighting equipment to

verify that preplanned firefighting procedures and appropriate firefighting techniques

were used, and to verify that the directions of the fire brigade leader were thorough,

clear, and effective. The inspectors attended the critique to confirm that appropriate

feedback on performance was provided to brigade members and to ensure that areas

for improvement were properly identified for licensee follow-up. In preparing for and

evaluating the drill the inspectors reviewed the preplanned drill scenario, Drill Number

99-F-RB-02 (Fire in Motor Control Center 2XDA), and the fire plan for the area as

documented in 2PFP-RB, Reactor Building Prefire Plans.

b. Findings

No findings of significance were identified.

1R11 Licensed Operator Requalification

b. Inspection Scope

The inspectors observed licensed operator performance and reviewed the associated

training documents during simulator training sessions for cycle 2003-04. This simulator

4

observation and review included an evaluation of emergency operating procedure and

abnormal operating procedure utilization. The inspectors reviewed Procedure OTPP-

200, Licensed Operator Continuing Training (LOCT) Program, to verify that the program

ensures safe power plant operation. The scenarios tested the operators ability to

respond to a hydraulic control unit low pressure, a conventional service water leak,

failure of an electro-hydraulic control pressure regulator, failure of the reactor protection

system to scram, loss of 4 kilovolt buses 2D and 3E, and a large break loss of coolant

accident. The inspectors reviewed the operators activities to verify consistent clarity

and formality of communication, conservative decision-making by the crew, appropriate

use of procedures, and proper alarm response. Group dynamics and supervisory

oversight, including the ability to properly identify and implement appropriate TS actions,

regulatory reports, and notifications, were observed. The inspectors reviewed simulator

scenario LORX-12 which documented the associated observed simulator training

scenario.

b. Findings

No findings of significance were identified.

1R12 Maintenance Effectiveness

a. Inspection Scope

For the equipment issues described in work documents listed below, the inspectors

reviewed the licensees implementation of the Maintenance Rule (10 CFR 50.65) with

respect to the characterization of failures, the appropriateness of the associated

Maintenance Rule a(1) or a(2) classification, and the appropriateness of the associated

a(1) goals and corrective actions. The inspectors also reviewed operations logs and

licensee event reports to verify unavailability times of components and systems, if

applicable. Licensee performance was evaluated against the requirements of

Procedure ADM-NGG-0101, Maintenance Rule Program. The inspectors also reviewed

deficiencies related to the work activities listed below to verify that the licensee had

identified and resolved deficiencies in accordance with Procedure CAP-NGGC-0200,

Corrective Action.

  • WOs 440591 and 440593 - Containment atmosphere control (CAC) flow control

valves 2717 and 2720 failures to stoke fully

release

b. Findings

No findings of significance were identified.

5

1R13 Maintenance Risk Assessments and Emergent Work Evaluation

a. Inspection Scope

The inspectors reviewed the licensees implementation of 10 CFR 50.65 (a)(4)

requirements during scheduled and emergent maintenance activities using Procedure

OAP-025, BNP Integrated Scheduling and Technical Requirements Manual (TRM)

5.5.13, Configuration Risk Management Program. The inspectors reviewed the

effectiveness of risk assessments performed prior to changes in plant configuration for

maintenance activities (planned and emergent). The review was conducted to verify

that, upon unforseen situations, the licensee had taken the necessary steps to plan and

control the resultant emergent work activities. The inspectors reviewed the applicable

plant risk profiles, work week schedules, and maintenance work orders for the following

OOS equipment:

  • AR 98294 Failure of torus purge exhaust valve (1-CAC-V7) to meet

in-service test stroke time requirements results in a yellow

risk window due to the unavailability of the large

suppression pool vent and hardened wetwell vent paths

  • AR 98771 Tripping of the 1A-2 battery charger output breaker results

in a yellow risk window

  • 0MST-DG501R3 Preplanned 72-month inspection of emergency diesel

generator (EDG) #3 results in a yellow risk window, BNP

Risk Profile Week 29

of EDG #4 planned outage during work week 34

  • AR 103914103914 Unit 2 A 250-volt battery positive bus ground and

subsequent troubleshooting activities occurring on

September 7, 2003

scope reduction due to the approach of Hurricane Isabel

during Work Week 37

meeting TS 3.8.6 Category C limits

b. Findings

No findings of significance were identified.

1R14 Operator Performance During Non-Routine Plant Evolutions and Events

a. Inspection Scope

The inspectors observed and monitored Unit 1 control room personnel actions during

the power decrease and ascension associated with the forced outage on July 1, 2003,

due to drywell leakage in excess of that allowed by TS. Operator actions were observed

prior to the forced outage during drywell valve back seating efforts to mitigate the

leakage. The purpose of the review was to verify the following: (1) the power changes

were performed in accordance with Procedure 0GP-12, Power Changes, (2) the

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appropriate TS was entered during the back seating activities, and (3) control room

operations personnel were provided with guidance on the control of plant equipment and

system status in accordance with Operating Instruction 0OI-01.08, Control of Equipment

and System Status.

b. Findings

No findings of significance were identified.

1R15 Operability Evaluations

a. Inspection Scope

The inspectors reviewed the operability evaluations associated with six issues, listed

below, which affected risk significant systems or components to assess, as appropriate:

(1) the technical adequacy of the evaluations; (2) the justification of continued system

operability; (3) any existing degraded conditions used as compensatory measures; (4)

the adequacy of any compensatory measures in place, including their intended use and

control; and (5) where continued operability was considered unjustified, the impact on

TS limiting conditions for operations (LCOs) and the risk significance. In addition to the

reviews, discussions were conducted with the applicable system engineer regarding the

ability of the system to perform its intended safety function.

to address potential vortexing and air entrainment while aligned to

the condensate storage tank as a suction source

  • AR 99205 Coolant leak from motor-driven fire pump heat exchanger
  • AR 98654 Vital battery 1A-2 battery charger main supply breaker tripped
  • AR 104326104326Vital battery 1A-1 cell #53 cracked with small leak
  • EER 940217 Engineering evaluation report to downgrade the 24/48 volt DC

system to Quality Class B

b. Findings

No findings of significance were identified.

1R16 Operator Work-Arounds (OWAs)

a. Inspection Scope

The inspectors reviewed the status of OWAs for Units 1 and 2 to determine if the

functional capability of the system or operator reliability in responding to an initiating

event was affected. The review was to evaluate the effect of the OWA on the operators

ability to implement abnormal or emergency operating procedures during transient or

event conditions. The inspectors compared licensee actions to the requirements of

Procedure 0OI-01.08, Control of Equipment and System Status and held discussions

with operations personnel related to the OWAs reviewed.

7

The two OWAs reviewed were:

  • OWA-403, Auxiliary Operator or Instrumentation and Control Technician Isolate

Three High Pressure Oil Switches Prior to Resetting a Reactor Feedwater Pump

Turbine or Starting a Reactor Feedwater Pump Turbine Oil Pump. A

modification on Unit 2 has replaced switches and the Unit 1 Modification will be

performed in the 2004 outage (See Integrated Inspection Report Numbers 50-

325/03-03 and 50-324/03-03)

  • OWA-375, Leak By Valves Upstream of Feedwater Stop Valve Causes Rapid

Injection of Cold Water when Opening per GP-02

b. Findings

No findings of significance were identified.

1R17 Permanent Plant Modifications

a. Inspection Scope

The inspectors reviewed a permanent plant modification (WO 326591) that removed

pneumatic controls located in the E3 switchgear room and replaced them with a

temperature switch. The inspectors reviewed the design adequacy of the modification

for material compatibility which included functional properties, environmental

qualification, and seismic evaluation. One purpose of the review was to verify that the

replacement switch performance characteristics met the design bases and the design

assumptions. Another purpose was to verify that modification preparation, staging, and

implementation did not impair emergency/abnormal operating procedure actions and

key safety functions. The inspectors also reviewed the modification to verify that the

post-modification testing would establish operability and that unintended system

interactions would not occur, and that testing demonstrated that the modification

acceptance criteria were met.

1R19 Post Maintenance Testing

a. Inspection Scope

For the post maintenance tests and maintenance activities listed below, the inspectors

reviewed the test procedure and witnessed the testing and/or reviewed test records to

confirm that the scope of testing adequately verified that the work performed was

correctly completed, and that the test demonstrated that the affected equipment was

capable of performing its intended function and was operable in accordance with TS

requirements. The inspectors reviewed the licensees actions against the requirements

in Procedure 0PLP-20, Post Maintenance Testing Program.

maintenance on Unit 2 B core spray system

  • 0PT-10.1.8, RCIC System Valve Operability Test following channel calibrations

on Unit 2 RCIC

8

maintenance on system damper 1-VA-1D-BFV-RB-MO per WO 71178

replacement on scram solenoid pilot valves 2-C12-SV-117/118 (Unit 2 control

rod 42-43) per WO 434466

  • WO 440591, post-maintenance test of CAC system flow controller 2-CAC-FCU-

2717 following circuit board replacement

  • AR 98654, post-maintenance test of the battery charger amplifier board

replacement

b. Findings

No findings of significance were identified.

1R20 Refueling and Other Outage Activities

a. Inspection Scope

The inspectors monitored portions of the Unit 1 TS required shutdown that commenced

on June 30, 2003, due to high drywell unidentified leakage. The inspectors verified that

the requirements of General Plant Operating Procedure 0GP-05, Unit Shutdown, were

met. Additionally the inspectors reviewed the data package of Procedure 1PT-01.7,

Heatup/cooldown Monitoring, to verify that vessel cooldown rates were not exceeded.

The inspectors monitored the heatup and startup activities following the Unit 1 forced

outage. The inspectors reviewed Procedures 0GP-01, Pre-startup Checklist, and 0GP-

02, Approach to Criticality and Pressurization of the Reactor to ensure that control room

operators satisfied procedural requirements. In addition, the inspectors reviewed TS,

license conditions, commitments, and administrative procedural prerequisites for mode

changes to verify that the requirements for changing the plant configurations were met.

The changing plant configurations observed by the inspectors included the reactor

startup, the approach to criticality, and portions of the power ascension.

b. Findings

No findings of significance were identified.

1R22 Surveillance Testing

1. Routine Surveillance Testing

a. Inspection Scope

The inspectors either observed surveillance tests or reviewed test data for the risk

significant SSC surveillance listed below to verify the tests met TS surveillance

requirements, UFSAR commitments, in-service testing (IST), and licensee procedural

requirements. The inspectors assessed the effectiveness of the tests in demonstrating

that the SSCs were operationally capable of performing their intended safety functions.

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  • Periodic Test 0PT-10.1.1, RCIC System Operability Test, performed on Unit 2
  • Periodic Test 1PT-01.7, Heatup/cooldown Monitoring
  • Periodic Test 0PT-14.2.1, Single Rod Scram Insertion Times Test, performed on

Unit 2

  • Periodic Test OPT-12.2B, EDG #2 monthly load test

b. Findings

No findings of significance were identified.

2. Inservice Surveillance Testing

a. Inspection Scope

The inspectors observed the performance of Periodic Test 0PT-08.2b, Low Pressure

Coolant Injection (LPCI)/Residual Heat Removal (RHR) Operability Test-Loop B,

performed on Unit 2. The inspectors evaluated the effectiveness of the licensees

American Society of Mechanical Engineers (ASME)Section XI testing program to

determine equipment availability and reliability. The inspectors evaluated selected

portions of the following areas: (1) testing procedures; (2) acceptance criteria; (3) testing

methods; (4) compliance with the licensees in-service testing program, TS, selected

licensee commitments, and code requirements; (5) range and accuracy of test

instruments; and (6) required corrective actions. The inspectors also assessed any

applicable corrective actions taken.

b. Findings

No findings of significance were identified.

1R23 Temporary Plant Modifications

a. Inspection Scope

The inspectors reviewed Plant Operating Manual 0PLP-22, Temporary Changes, to

assess implementation of the below listed temporary modifications. The inspectors

reviewed these temporary modifications to verify that the modifications were properly

installed and whether they had any effect on system operability. The inspectors also

assessed drawings and procedures for appropriate updating and post-modification

testing.

phase B isophase bus duct

b. Findings

No findings of significance were identified.

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Cornerstone: Emergency Preparedness

1EP6 Drill Evaluation

a. Inspection Scope

The inspectors observed two site emergency preparedness training evolutions

conducted on July 15, 2003, and September 2, 2003. The inspectors reviewed the drill

scenarios narrative to identify the timing and location of classification, notification, and

protective action recommendation (PAR) development activities. The inspectors

evaluated each drills conduct from the control room simulator, technical support center,

and the emergency operations facility. During the drills, the inspectors assessed the

adequacy of event classification and notification activities. The inspectors observed the

licensees post-drill critiques and evaluated the licensees self assessments of

classification, notification, and protective action recommendation development. The

inspectors assessed the licensees evaluation of each drills performance with respect to

performance indicators. To assess the ability of the licensee to identify and correct

problems the inspectors reviewed ARs 105705 and 105706 which documented drill

performance deficiencies and improvement items from the observed drill.

b. Findings

No findings of significance were identified.

4. OTHER ACTIVITIES

4OA1 Performance Indicator Verification

a. Inspection Scope

The inspectors reviewed the performance indicator (PI) data submitted in July 2003 to

the NRC since the last verification inspection was performed. A sample of plant records

and data was reviewed and compared to the reported data to verify the accuracy of the

performance indicators. The licensees corrective action program records were also

reviewed to determine if any problems with the collection of PI data had occurred. PI

definitions and guidance contained in Nuclear Energy Institute (NEI) 99-02, Regulatory

Assessment Performance Indicator Guideline, Revision 2 were utilized.

The inspectors reviewed the following Units 1 and 2 PIs for the period July 2002 to June

2003:

  • Safety System Functional Failures

The following documents were reviewed:

  • Control room operating logs
  • NRC inspection reports issued during the review period

11

  • Licensees data bases for the PIs listed above
  • Nuclear Generating Group Standard Procedure REG-NGGC-0009, NRC

Performance Indicator

  • NEI 99-02 Regulatory Assessment Performance Indicator Guideline
  • Licensee Event Reports

b. Findings

No findings of significance were identified.

4OA2 Problem Identification and Resolution

a. Inspection Scope

The inspectors performed an in-depth annual sample review of selected ARs to

determine whether conditions adverse to quality were addressed in a manner that was

commensurate with the safety significance of the issue. The inspectors reviewed the

actions taken to verify that the licensee had adequately addressed the following

attributes:

  • Complete, accurate, and timely identification of the problem
  • Evaluation and disposition of operability and reportability issues
  • Consideration of previous failures, extent of condition, generic or common cause

implications

  • Prioritization and resolution of the issue commensurate with the safety

significance

  • Identification of the root cause and contributing causes of the problem
  • Identification and implementation of corrective actions commensurate with the

safety significance of the issue

The following issues and associated corrective actions were reviewed:

strainer differential pressure

failures

c. Findings and Observations

Introduction: A Green NCV was identified for inadequate corrective actions to prevent

the recurrence of service water pump discharge strainer blowdown lines from clogging.

Description: On July 8, 1999, the licensee identified a significant adverse condition

(AR 07149). The licensee noted several instances when the blowdown lines of the

service water (nuclear and conventional) pump discharge strainers became clogged with

oyster shells, rendering the pump impaired and/or inoperable. The service water pumps

are deep-well pumps and take suction on the service water intake structure bays. The

pumps provide cooling water to various safety-related (i.e. EDGs and RHR systems)

and non-safety-related loads. The licensee determined that the root cause was due to

12

inadequate cleaning of the service water pump bays, and implemented a yearly

preventive maintenance cleaning of the bays. The AR was closed on

August 24, 2000.

On October 10, 2002, the licensee identified another significant adverse condition (AR

74020), again identifying several instances of service water pump inoperabilities due to

the pump strainer blowdown line becoming clogged with oyster shells. In both of the

above mentioned issues, the licensee identified a contributing cause as the

formation/existence of oyster shells in the vicinity of the service water pump suction.

In May 2003, the inspectors questioned the status of the root cause analysis and

corrective actions of AR 74020. At that time, corrective actions had not been fully

implemented. The inspectors noted that the root cause was determined to be

inadequate cleaning of the service water pump bays. The inspectors questioned the

promptness and adequacy of the licensees corrective action plan given the fact that

three functional failures had occurred during the first three months of 2003. The

licensee subsequently reevaluated the root cause evaluation and corrective actions of

AR 74020, and identified oyster growth on the pump casings as an additional root

cause. Past cleanings of the pump bays did not include cleaning of the deep-well pump

exterior casings. The licensee implemented increased monitoring of strainer differential

pressure to detect possible blowdown line clogging at an early stage, thus reducing

pump functional failures. Additional corrective actions were planned to clean the pump

casings concurrent with bay cleanings. Other corrective actions and enhancements

were planned to improve system reliability.

Analysis: This finding is greater than minor because it resulted in an increase in the

likelihood of loss of nuclear and conventional service water initiating events. In addition,

the mitigating systems cornerstone objective to ensure reliability, availability, and

capability of systems that respond to initiating events was affected by equipment

performance. The deficiency was evaluated using the out-of-service times for the

nuclear and conventional services water pumps for the past year. A Significance

Determination Process analysis determined the finding to be of very low safety

significance (Green) due to the relatively short duration of unavailability of the pumps.

Enforcement: 10 CFR 50, Appendix B, Criterion XVI, Corrective Action, requires in part,

that measures be established to assure that conditions adverse to quality are promptly

identified and corrected. In the case for significant conditions adverse to quality, the

measures shall assure the cause of the condition is determined and corrective actions

taken to preclude repetition. The corrective actions of ARs 07149 and 74020 failed to

preclude repetitive functional failures of nuclear and conventional service water pumps

due to discharge strainer blowdown line clogging. This resulted in six pump failures in a

twelve month time-frame, between October 2002 and September 2003. Because the

failure of the corrective actions to prevent repetition is of very low safety significance

and has been entered into the corrective action program (revision to AR 74020), this

violation is being treated as an NCV, consistent with Section VI.A of the NRC

Enforcement Policy: NCV 50-324,325/2003-05-01, Inadequate Corrective Actions for

Service Water Strainer Blowdown Line Clogging.

13

4OA3 Event Follow-up

1. Unusual Event Due to Hurricane Warning

a. Inspection Scope

At 10:40 p.m. on September 16, 2003, the site declared an Unusual Event due to the

issuance of a hurricane warning for the Cape Fear Region of North Carolina. The

inspectors reviewed Plant Emergency Procedure 0PEP-02.1, Initial Emergency Actions,

to verify the licensees actions to classify and make timely notification were consistent

with site emergency plan requirements. The inspectors reviewed plant status including

the availability of mitigating systems and the effect of storm conditions on the plant. The

inspectors assessed licensee performance with respect to the licensees staffing of the

emergency response organization, provisions for the relief of plant operators, and plant

damage assessment. During the approach of the storm the inspectors communicated

plant status to the Region II Incident Response Center. At 5:40 p.m. on September 18,

2003, the licensee exited the Unusual Event due to the lifting of the hurricane warning

for the Cape Fear Region. See Section 1R01 for additional inspector activities

associated with adverse weather preparations.

b. Findings

No findings of significance were identified.

2. (Closed) Licensee Event Report (LER) 50-324/2003-01: Main Steam Line Drain

Isolation Valve Local Leak Rate Test Failures. During the Spring 2003 Unit 2 refueling

outage, the results of local leak rate testing of the main stream line drain inboard and

outboard isolation valves (2-B21-F016 and 2-B21-F019) determined that the valves

would not pressurize. Due to the inability to pressurize the containment penetration, the

ability to quantify the leak rate of the penetration was beyond the ability of the licensees

test method. Therefore, the licensee conservatively assumed a direct path of a 3-inch

nominal pipe size for containment leak rate determination. This method of quantifying

the leak rate, administratively required by the licensees Appendix J program, resulted in

a calculated leak rate that exceeded the TS primary containment leak rate limit.

The outboard isolation valve was refurbished by replacing the valve steam and disc

assemblies. Only small defects of the valve disc were observed. The inboard isolation

valve, a limit-seated valve, needed only a minor limit switch adjustment to achieve

satisfactory leak rate results. Although the valves were not leak tight, the valves were

capable of closing and reducing the release of radioactive gases. Based on this

information and the demonstrated ability of the valves to close, the inspector concluded

that the method for calculating the penetration leak rate, was conservative. The valves

were classified as a(1) in the licensees Maintenance Rule Program. The licensee

planned to replace the valves with a design that will provide better isolation capability.

The licensee also planned to install an additional block valve and a test connection in

the system that will facilitate local leak rate testing. This event did not constitute a

violation of NRC requirements due to the uncertainty on when the containment

penetration leakage problems occurred, with respect to the allowed out-of-service time.

14

The licensee documented the issue in the corrective action program as AR 88364. This

LER is closed.

3. (Closed) LER 50-324/2003-02: Reactor Protection System Instrumentation Out of

Calibration Results in Operation Prohibited by Technical Specifications. During the

Spring 2003 Unit 2 refueling outage, maintenance technicians recorded as-found

calibration setpoints on four-of-eight inboard and outboard main steam isolation valve-

closure reactor protection system position limit switches exceeding the TS allowable

value. The data was collected using a new licensee calibration method which was more

repeatable and removed human factors associated with the previously used method.

The previous method, which was used to set the limit switches during previous outages,

relied on visual observations and coordination between personnel in different locations

to measure the limit switch setpoint. The inspector noted that the previous method used

by the licensee was consistent with industry practice.

The main steam isolation valve-closure reactor trip function is intended to initiate a

scram prior to a significant reduction in steam flow thus reducing the severity of the

subsequent pressure transient and its effect on fuel thermal limits. The licensees

evaluation of the as-found condition determined that the condition did not appreciable

decrease the fuel thermal margin nor did it significantly impact peak transient system

pressurization. The main steam isolation valve-closure reactor trip function is not

credited in the plants over-pressure analysis.

Because the new calibration method was not available during the previous Unit 1

outage, the inspector reviewed the licensees assessment of test data. The inspector

concluded that there was a reasonable assurance of operability for the Unit 1 limit

switches due to the existence of more margin between the as-left measured setpoint

and the TS allowable value. This event did not constitute a violation of NRC

requirements due to the uncertainty as to what effect the more conservative nature of

the revised calibration methodology had on actual as-found instrument calibration

setpoints. The licensee documented the event in the corrective action program as AR

89077. This LER is closed.

4. (Closed) LER 50-324/2003-03: Unit 2 Scram During Startup Due to Electro Hydraulic

Control (EHC) System Malfunction. The cause of the event was determined to be an

intermittent error signal from an EHC card that was improperly engaged in its hardware

slot in the EHC pressure control circuitry. The licensee found the steam line resonance

compensator (SLRC) card for the B EHC pressure regulator was not fully seated.

Although the card was not removed for maintenance during the Spring 2003 refueling

outage, other cards in the cabinet had been removed and reinstalled. Prior to operation,

all cards were checked for proper engagement. The licensees practice for verifying

proper engagement was to apply manual pressure to cards that had been removed and

perform visual inspection of all other cards. Due to the design and arrangement of the

SLRC cards, the licensee determined that manual seating and verification of proper

seating was less than optimal. The licensee planned a procedure revision to add detail

to the restoration steps for EHC cards to assure proper engagement for all cards

following maintenance activities. The LER was reviewed by the inspectors and no

findings of significance were identified. This event did not constitute a violation of NRC

15

requirements. The licensee documented the event in the corrective action program as

AR 89705. This LER is closed.

4OA5 Other

Review of World Association of Nuclear Operators (WANO) Interim Report

The inspectors reviewed a WANO Interim Report for the Brunswick Steam Electric

Plant, dated August 14, 2003. The review determined that the results of the WANO

report were generally consistent with the results of similar evaluations conducted by the

NRC. The inspectors determine that no additional Regional follow-up concerning the

results of the WANO report was warranted.

4OA6 Meetings, Including Exit

Exit Meeting Summary

On September 17, 2003, the resident inspectors presented the inspection results to

Mr. J. Keenan and other members of his staff. The inspectors confirmed that

proprietary information was not provided or examined during the inspection.

SUPPLEMENTAL INFORMATION

KEY POINTS OF CONTACT

Licensee Personnel:

A. Brittain, Manager Security

E. Conway, Senior Nuclear Security Specialist

W. Dorman, Manager Nuclear Assessment

C. Elberfeld, Lead Engineer, Technical Support

N. Gannon, Director of Site Operations

J. Gawron, Training Manager

D. Hinds, Manager Brunswick Engineering Support Section

J. Keenan, Site Vice President

D. Makosky, Lead Nuclear Security Specialist

W. Noll, Plant General Manager

E. ONeil, Manager Site Support Services

H. Wall, Manager Maintenance

E. Quidley, Manager Outage and Scheduling

M. Williams, Manager Operations

NRC Personnel:

P. Fredrickson, Branch Chief, Division of Reactor Projects (DRP), Region II (RII)

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

None

Opened and Closed

50-324,325/2003-05-01 NCV Inadequate Corrective Actions for Service Water Strainer

Blowdown Line Clogging (Section 4OA2)

Closed

50-324/2003-01 LER Main Steam Line Drain Isolation Valve Local Leak Rate

Test Failures (Section 4OA3.2)

50-324/2003-02 LER Reactor Protection System Instrumentation Out of

Calibration Results in Operation Prohibited by Technical

Specifications (Section 4OA3.3)

50-324/2003-03 LER Unit 2 Scram During Startup Due to Electro Hydraulic

Control System Malfunction (Section 4OA3.4)

Discussed

None

Attachment