ML023020655

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IR 05000263-02-005, on 07/01-09/30/2002; Nuclear Management Co, LLC; Monticello Nuclear Generating Plant. Maintenance Risk Assessments & Emergent Work Control
ML023020655
Person / Time
Site: Monticello Xcel Energy icon.png
Issue date: 10/25/2002
From: Burgess B
NRC/RGN-III/DRP/RPB2
To: Forbes J
Nuclear Management Co
References
IR-02-004 IR-02-005
Download: ML023020655 (42)


See also: IR 05000263/2002005

Text

October 25, 2002

Mr. J. Forbes

Site Vice-President

Monticello Nuclear Generating Plant

Nuclear Management Company, LLC

2807 West County Road 75

Monticello, MN 55362-9637

SUBJECT:

MONTICELLO NUCLEAR GENERATING PLANT

USNRC INTEGRATED INSPECTION REPORT 50-263/02-05

Dear Mr. Forbes:

On September 30, 2002, the U.S. Nuclear Regulatory Commission (USNRC) completed an

integrated inspection at your Monticello Nuclear Generating Plant. The enclosed report

documents the inspection findings which were discussed on October 3, 2002, with Mr. Jack

Purkis and other members of your staff.

The inspection examined activities conducted under your license as they relate to safety and

compliance with the Commissions rules and regulations and with the conditions of your license.

The inspectors reviewed selected procedures and records, observed activities, and interviewed

personnel.

Based on the results of this inspection, the USNRC identified one finding of very low safety

significance (Green) and an associated Non-Cited Violation. If you contest the subject or

severity of this Non-Cited Violation, you should provide a response within 30 days of the date of

this inspection report, with a basis for your denial, to the U. S. Nuclear Regulatory Commission,

ATTN: Document Control Desk, Washington, DC 20555-0001, with copies to the Regional

Administrator, Region III, 801 Warrenville Road, Lisle, IL 60532-4351; the Director, Office of

Enforcement, U. S. Nuclear Regulatory Commission, Washington, DC 20555-0001; and the

Resident Inspectors' Office at the Monticello Nuclear Generating Station.

A previous inspection report, 50-263/02-04, dated July 24, 2002, contained an administrative

error in the table of "Items Opened, Closed, and Discussed" on page 27. Please be advised

that NCV No. 50-263/02-04-02 was listed in the "Closed" section in error. No such enforcement

item was ever opened.

In response to the terrorist attacks on September 11, 2001, the USNRC issued an Order and

several threat advisories to commercial power reactors to strengthen licensees' capabilities and

readiness to respond to a potential attack. The USNRC established a deadline of

September 1, 2002, for licensees to complete modifications and process upgrades required by

the order. In order to confirm compliance with this order, the USNRC issued Temporary

Instruction 2515/148, and over the next year the USNRC will inspect each licensee in

accordance with this Temporary Instruction. The USNRC continues to monitor overall security

J. Forbes

-2-

controls and may issue additional temporary instructions or require additional inspections

should conditions warrant.

In accordance with 10 CFR 2.790 of the USNRCs "Rules of Practice," a copy of this letter

and its enclosure will be available electronically for public inspection in the USNRC Public

Document Room or from the Publicly Available Records (PARS) component of USNRCs

document system (ADAMS). ADAMS is accessible from the USNRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA by Geoffrey Wright Acting for/

Bruce L. Burgess, Chief

Branch 2

Division of Reactor Projects

Docket No. 50-263

License No. DPR-22

Enclosure:

Inspection Report 50-263/02-05

cc w/encl:

J. Purkis, Plant Manager

R. Anderson, Executive Vice President

and Chief Nuclear Officer

Nuclear Asset Manager

Site Licensing Manager

Commissioner, Minnesota Department of Health

J. Silberg, Esquire

Shaw, Pittman, Potts, and Trowbridge

R. Nelson, President

Minnesota Environmental Control Citizens

Association (MECCA)

Commissioner, Minnesota Pollution Control Agency

D. Gruber, Auditor/Treasurer

Wright County Government Center

Commissioner, Minnesota Department of Commerce

P. Marker, Office of Attorney General

DOCUMENT NAME: C:\\ORPCheckout\\FileNET\\ML023020655.wpd

To receive a copy of this document, indicate in the box: "C" = Copy without attachment/enclosure "E" = Copy with attachment/enclosure "N" = No copy

OFFICE

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NAME

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DATE

10/24/02

10/25/02

OFFICIAL RECORD COPY

J. Forbes

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U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket No:

50-263

License No:

DPR-22

Report No:

50-263/02-05

Licensee:

Nuclear Management Company, LLC

Facility:

Monticello Nuclear Generating Plant

Location:

2807 West Highway 75

Monticello, MN 55362

Dates:

July 1 through September 30, 2002

Inspectors:

S. Burton, Senior Resident Inspector

D. Kimble, Resident Inspector

J. Adams, Senior Resident Inspector - Prairie Island

R. Jickling, Emergency Preparedness Inspector

M. Mitchell, Radiation Specialist

G. Wright, Project Engineer

Approved by:

Bruce L. Burgess, Chief

Branch 2

Division of Reactor Projects

2

SUMMARY OF FINDINGS

IR 05000263-02-05; Nuclear Management Company, LLC; on 07/01-09/30/2002, Monticello

Nuclear Generating Plant. Maintenance Risk Assessments and Emergent Work Control.

This report covers a 3 month period of baseline resident inspection and announced baseline

inspections in radiation protection and emergency preparedness. The inspections were

conducted by resident inspectors and Region III inspectors. One Green finding was identified.

The significance of most findings is indicated by their color (Green, White, Yellow, Red) using

Inspection Manual Chapter (IMC) 0609 Significance Determination Process (SDP). Findings

for which the SDP does not apply may be "Green," or be assigned a severity level after USNRC

management review. The USNRC's program for overseeing the safe operation of commercial

nuclear power reactors is described in NUREG-1649, "Reactor Oversight Process," Revision 3,

dated July 2000.

A.

Inspection Finding

Cornerstone: Barrier Integrity

Green. A finding and an associated Non-Cited Violation (NCV) for failure to follow

applicable procedural guidance as required by Technical Specifications were identified

by NRC inspectors. The finding and NCV were associated with a loss of spent fuel pool

cooling which resulted from an improper licensee valve tagout/clearance operation.

Because the decay heat load in the spent fuel pool was relatively low, the spent fuel

pool temperature only increased from 90.5 degrees Fahrenheit to approximately

96.5 degrees Fahrenheit and the event involved only the fuel cladding barrier, the

finding was determined through a Phase 1 SDP to be of very low safety significance and

within the licensee response band. (Section 1R13)

B.

Licensee Identified Violations

No violations of significance were identified.

3

REPORT DETAILS

Summary of Plant Status

The plant began the inspection period operating at full power. On August 4, 2002, operators

were forced to reduce power to approximately 90 percent in response to problems with the

"D" demineralizer vessel in the condensate system. Full power operation was resumed later

that same day. On August 10, 2002, power was reduced to approximately 75 percent to

facilitate normal periodic main steam valve testing and control rod pattern adjustments. Full

power operation was resumed again on August 11, 2002. The plant operated at or near full

power for the remainder of the inspection period.

1.

REACTOR SAFETY

Cornerstones: Initiating Events, Mitigating Systems, Barrier Integrity, and

Emergency Preparedness

1R04

Equipment Alignment (71111.04)

.1

Partial Train/System Alignment Verification

a.

Inspection Scope

The inspectors performed a partial walkdown of the following equipment trains to verify

operability and proper equipment lineup. These systems were selected based upon risk

significance, plant configuration, system work or testing, or inoperable or degraded

conditions.

Division II Low Pressure Coolant Injection (LPCI) with Division I Out-of-Service

for Routine Maintenance (Week Ending 9/14)

Vital Electrical Distribution While Stand-by Liquid Control System Was Out of

Service for Surveillance Testing (Week Ending 7/13)

Reactor Core Isolation Cooling (RCIC) During Performance of Emergency Core

Cooling System (ECCS) Initiation Sensor Testing (Week Ending 9/27)

The inspectors verified the position of critical redundant equipment and looked for any

discrepancies between the existing equipment lineup and the required lineup.

b.

Findings

No findings of significance were identified.

4

.2

Semiannual Complete System Alignment Verification

a.

Inspection Scope

Due to the systems risk significance, the inspectors selected the RCIC system for a

complete walkdown. The inspectors walked down the system to verify mechanical and

electrical equipment lineups, component labeling, component lubrication, component

and equipment cooling, hangers and supports, operability of support systems, and to

ensure that ancillary equipment or debris did not interfere with equipment operation.

(Week Ending 7/20)

b.

Findings

No findings of significance were identified.

1R05

Fire Protection (71111.05)

.1

Quarterly Fire Zone Inspections

a.

Inspection Scope

The inspectors walked down multiple plant areas important to safety to assess the

material condition of reactor plant active and passive fire protection systems and

features and to look for any fire protection issues. The inspectors selected several

areas containing systems, structures, or components that the licensee identified as

important to reactor safety. (7/15 through 7/27)

Fire Zone A.3-13-A, Lube Oil Storage Tank Room

Fire Zone A.3-13-B, Reactor Feed Pump and Lube Oil Reservoir Room

Fire Zone A.3-13-C, Turbine Building 911' Elevation East Motor Control Center

(MCC) Area

Fire Zone A.3-15-B, No. 11 Diesel Generator Room and Day Tank Rooms

Fire Zone A.3-18-A, Hot Machine Shop

Fire Zone A.3-18-B, Oil Drum Storage Room

Fire Zone A.3-20, Auxiliary Boiler Room

Fire Zone A.3-21, Radwaste Shipping Building

Fire Zone A.3-04-D, Standby Gas Treatment Room

The inspectors reviewed the control of transient combustibles and ignition sources, fire

detection equipment, manual suppression capabilities, passive suppression capabilities,

automatic suppression capabilities, and barriers to fire propagation.

5

b.

Findings

No findings of significance were identified.

.2

Annual Fire Drill Observation

a.

Inspection Scope

On September 1, 2002, the inspectors conducted an annual observation of the stations

fire brigade during a drill which simulated a lubricating oil fire on the turbine building

911 elevation in and around the area of MCC 133. The inspectors evaluated the

readiness of the licensees personnel to prevent and fight fires by verifying that:

protective clothing/turnout gear was properly donned; self-contained breathing

apparatus equipment was properly worn and used; fire hose lines were capable of

reaching all necessary fire hazard locations, the lines were laid out without flow

constrictions, the hoses were simulated being charged with water, and the nozzles were

pattern (flow stream) tested prior to entering the fire area; the fire area was entered in a

controlled manner; sufficient fire fighting equipment was brought to the scene by the fire

brigade; the fire brigade leaders directions were thorough, clear, and effective;

communications with plant operators and between fire brigade members were efficient

and effective; the fire brigade checked for fire victims and for fire propagation into other

plant areas; effective smoke removal operations were simulated; fire fighting pre-plan

strategies were utilized; and the drill scenario was followed and the drill objectives met.

b.

Findings

No findings of significance were identified.

1R06

Flood Protection Measures (71111.06)

a.

Inspection Scope

Over several weeks in August 2002, the inspectors reviewed the licensees flooding

mitigation plans and equipment to determine consistency with design requirements and

risk analysis assumptions. Specifically, the inspectors conducted a review of the

licensees plans and equipment intended to control internal flooding within the

safety-related intake structure. Applicable walkdowns and reviews were performed that

considered design measures, seals, drain systems, contingency equipment condition,

availability of temporary equipment and barriers, performance and surveillance tests,

procedural adequacy, and planned compensatory measures.

b.

Findings

No findings of significance were identified.

6

1R11

Licensed Operator Requalification Program (71111.11)

a.

Inspection Scope

On September 4, 2002, the inspectors observed a training crew during an evaluated

simulator scenario and reviewed licensed operator performance in mitigating the

consequences of events. The scenario included an inadvertent initiation of RCIC, a loss

and subsequent recovery of a load center, and an accidental containment isolation

accompanied by a failure of control rods to insert. The transient resulted in the

operating crew implementing multiple emergency operating procedures while

responding to the failure to scram and associated torus heating. Areas observed by the

inspectors included: clarity and formality of communications, timeliness of actions,

prioritization of activities, procedural adequacy and implementation, control board

manipulations, managerial oversight, emergency plan execution, simulator

configuration, and group dynamics.

b.

Findings

No findings of significance were identified.

1R12

Maintenance Effectiveness (71111.12)

a.

Inspection Scope

The inspectors reviewed the licensees handling of performance issues and the

associated implementation of the Maintenance Rule (10 CFR 50.65) to evaluate

maintenance effectiveness for the selected system. The following system was selected

based on being designated as risk significant under the Maintenance Rule, being in the

increased monitoring (Maintenance Rule category a(1)) group, or due to an inspector

identified issue or problem that potential impacted system work practices, reliability, or

common cause failures:

Instrument Air System Piping Leak and Repair (Weeks Ending 8/3 - 8/17)

The inspectors review included verification of the licensee's categorization of specific

issues, including evaluation of the performance criteria, appropriate work practices,

identification of common cause errors, extent of condition, and trending of key

parameters. Additionally, the inspectors reviewed the licensee's implementation of the

maintenance rule requirements, including a review of scoping, goal-setting, performance

monitoring, short-term and long-term corrective actions, functional failure determinations

associated with the condition reports reviewed, and current equipment performance

status.

b.

Findings

No findings of significance were identified.

7

1R13

Maintenance Risk Assessments and Emergent Work Control (71111.13)

a.

Inspection Scope

The inspectors reviewed and observed emergent work, preventive maintenance, or

planning for risk significant maintenance activities. The inspectors observed

maintenance or planning for the following activities or risk significant systems

undergoing scheduled or emergent maintenance:

Weekly Scheduling and Planning Meetings (All Weeks)

Outage Planning and Emergent Work Review (All Weeks)

Risk Management During Reactor Protection System Testing Combined With

Rescheduled Standby Liquid Control System Testing (Week Ending 7/13)

Risk Management During Identification and Resolution of Cooling Tower and

Basin Instrument Air System Leak (Weeks Ending 8/3 and 8/10)

Emergent Maintenance and Risk Management for Repair of 11 Control Rod

Drive Hydraulic Pump Leaking Casing (Week Ending 8/17)

Maintenance and Risk Management During Work on Fuel Pool Cooling System

and Subsequent Loss of Fuel Pool Cooling Event (Week Ending 8/24)

The inspectors also reviewed the licensee's evaluation of plant risk, risk management,

scheduling, and configuration control for these activities in coordination with other

scheduled risk significant work. The inspectors verified that the licensee's control of

activities considered assessment of baseline and cumulative risk, management of plant

configuration, control of maintenance, and external impacts on risk. In-plant activities

were reviewed to ensure that the risk assessment of maintenance or emergent work

was complete and adequate, and that the assessment included an evaluation of external

factors. Additionally, the inspectors verified that the licensee entered the appropriate

risk category for the evolutions.

b.

Findings

(1)

Introduction

A finding of very low safety significance (Green) and an associated NCV for failure to

follow applicable procedural guidance were identified by inspectors. The finding and

NCV were associated with the loss of spent fuel pool cooling which resulted from an

improper licensee valve tagout/clearance operation.

(2)

Description

On August 23, 2002, the licensee initiated a tagout to isolate the No. 12 fuel pool

filter/demineralizer for planned maintenance. Included in this tagout was valve

AO-2807, the drain valve for the in-service No. 11 fuel pool filter/demineralizer. As

8

indicated on the licensees spent fuel pool cooling system drawing, AO-2807 was a

normally closed, fail closed valve. Thus, the licensees tagout called for AO-2807 to be

tagged in the shut position with operating air removed from the valve.

When plant operators applied the tagout to AO-2807 and removed the valves operating

air, the valve unexpectedly moved to the open position. This immediately established a

drain path between the operating train of spent fuel cooling and the waste sludge tank in

the radwaste system. Approximately 10 minutes elapsed before operators in the field

were informed of the problem by the control room, returned to AO-2807, and reapplied

operating air to shut the valve. During this time, approximately 2000 gallons, or

25 percent of the available surge volume, was drained from the operating train of spent

fuel pool cooling to the radwaste system. Although actual spent fuel pool level was

never affected, the loss of inventory from the surge tank brought in multiple alarms in

the control room, including the spent fuel pool surge tank low-low level alarm, which

caused the operating spent fuel pool cooling pump to trip. Control room operators

immediately entered the abnormal operating procedure for loss of spent fuel pool

cooling. Recognizing that the decay heat load in the spent fuel pool was relatively small,

the operations crew was able to take well planned and deliberate steps to restore flow to

the spent fuel pool cooling system. Although spent fuel pool cooling flow was not

reestablished until almost 16 hours1.851852e-4 days <br />0.00444 hours <br />2.645503e-5 weeks <br />6.088e-6 months <br /> later because of ongoing maintenance on various

parts of the system, spent fuel pool temperature increased by only 6 degrees Fahrenheit

over that time due to the low amount of decay heat being produced by the irradiated fuel

in the pool.

Upon investigation of this event, the licensee identified that the licensed operators who

had prepared the tagout and the system engineer for the spent fuel pool cooling system

had missed critical information concerning the operation of AO-2807. General

precautions regarding AO-2807 listed in the licensees operating procedures for the

spent fuel cooling system warn personnel against removing air from the valve operator,

as the spring force is insufficient, by design, to maintain the valve in the closed position

against normal system pressure and flow. Additionally, the licensees investigation

revealed that special gagging devices were available specifically for AO-2807 to hold it

closed against system pressure and flow. However, these devices were in the

possession of a previous system engineer and neither the current system engineer nor

any of the operations personnel involved with the tagout had any knowledge of their

existence.

(3)

Analysis

With respect to the tagout for the isolation of No. 12 fuel pool filter/demineralizer, the

inspectors determined that the licensees failure to recognize established procedural

guidance regarding the inability of AO-2807 to remain in the closed position without

control air constituted a performance deficiency in accordance with USNRC Inspection

Manual Chapter (IMC) 0612, Appendix B, "Issue Dispositioning Screening." Further, the

inspectors determined that the loss of spent fuel pool cooling event which resulted from

this performance deficiency was more than minor in that it directly affected the objective

of the Barrier Integrity Reactor Safety Cornerstone.

9

With respect to the irradiated fuel in the spent fuel pool, the primary physical design

barrier which provides protection to the public is the fuel cladding. The spent fuel pool

cooling system is designed to remove decay heat and thereby maintain fuel cladding

integrity. Thus, the tagout error(s) by the licensee which resulted in the loss of the

in-service spent fuel pool cooling train had an effect on the fuel cladding temperature of

the spent fuel in the spent fuel pool. Specifically, the loss of the in-service train of spent

fuel pool cooling resulted in a measurable cladding temperature increase.

In order to determine the significance of the event, the inspectors performed a

Phase 1 SDP in accordance with IMC 0609, Appendix A, "Significance Determination of

Reactor Inspection Findings for At-Power Situations." The inspectors concluded that

because the decay heat load in the spent fuel pool was relatively low, the spent fuel pool

temperature only increased from 90.5 degrees Fahrenheit to approximately 96.5 degrees

Fahrenheit, and the event involved only the fuel cladding barrier, the finding was of very

low safety significance (Green) and within the licensee response band.

(4)

Enforcement

Technical Specification 6.5.A.1, via Regulatory Guide 1.33, Revision 2, Appendix A,

requires that the licensee establish and follow appropriately approved procedures for the

operation of the spent fuel pool cooling system. Contrary to this requirement, the

licensee failed to follow approved procedural guidance in Operations Manual Section

B.02.01-05 related to the operation of the AO-2807 valve when the valve was tagged in

the shut position with control air removed to support work on No. 12 fuel pool

filter/demineralizer on August 23, 2002. This violation is being treated as a NCV

consistent with Section VI.A of the USNRC Enforcement Policy (NCV 50-263/02-05-01).

The licensee has entered this issue into their corrective action program as CR 20027940.

Planned corrective actions include procedural and component database enhancements

regarding the use of this type of air operated valve as an isolation boundary, and

enhancements to the system engineer turnover process.

1R15

Operability Evaluations (71111.15)

a.

Inspection Scope

The inspectors reviewed the technical adequacy of the following operability evaluations to

determine the impact on Technical Specifications, the significance of the evaluations,

and to ensure that adequate justifications were documented.

12 Emergency Diesel Generator (EDG) Lube Oil Lead Content Increasing to the

Point of Additional Monitoring (Week Ending 8/10)

Main Steam Line Radiation Monitors Not Maintained as Safety-Related (Week

Ending 8/24)

Diesel Fire Pump Discharge Check Valve Inadequate Bolting (Week Ending 8/31)

Residual Heat Removal (RHR) Corner Room Calculation Assumptions

Inconsistent with Current Plant Operating Practices (Week Ending 8/31)

10

Operability evaluations were selected based upon the relationship of the safety-related

system, structure, or component to risk.

b.

Findings

No findings of significance were identified.

1R16

Operator Workarounds (71111.16)

a.

Inspection Scope

During the week ending September 21, 2002, the inspectors reviewed Operations

Challenge No.02-042, "Annunciator 7-B-17 For Vacuum 24 Inch Trip No. 2 Alarmed."

The inspectors reviewed the workarounds potential to impact the operators ability to

respond to a decreasing condenser vacuum situation.

b.

Findings

No findings of significance were identified.

1R17

Permanent Plant Modifications (71111.17)

a.

Inspection Scope

During the week ending August 24, 2002, the inspectors reviewed an alteration to the

control room emergency filtration train (EFT) charcoal filters to verify that the design

basis, licensing basis, and performance capability of the system was not degraded by the

alteration. The inspectors also verified that the alteration did not place the plant in an

unsafe configuration.

The inspectors considered the design adequacy of the alteration by performing a review

of the alterations impact on plant electrical requirements, material requirements and

replacement components, response time, control signals, equipment protection,

operation, failure modes, and other related process requirements.

b.

Findings

No findings of significance were identified.

1R19

Post-Maintenance Testing (71111.19)

a.

Inspection Scope

The inspectors selected the following post-maintenance activities for review. Activities

were selected based upon the structure, system, or components ability to impact risk.

No. 12 EDG Testing Following Speed Changer Motor Replacement (Week

Ending 7/6)

11

Post Maintenance Testing of RCIC Following Repairs to Leaking Components

(Week Ending 7/27)

Post Maintenance Testing Following Failure of HPCI Test Return Line Control Air

Supply (Week Ending 8/17)

Post Maintenance Testing Following Routine Scheduled Work on the Diesel Fire

Pump (Week Ending 8/24)

Post Maintenance Testing Following Routine Preventative Maintenance of

Division I RHR LPCI Inboard Isolation Valve, MO-2014 (Week Ending 9/14)

Post Maintenance Testing Following Routine Preventative Maintenance on No. 13

Residual Heat Removal Service Water (RHRSW) Pump Motor Cooler (Week

Ending 9/14)

The inspectors verified by witnessing the test or reviewing the test data that

post-maintenance testing activities were adequate for the above maintenance activities.

The inspectors reviews included, but were not limited to, integration of testing activities,

applicability of acceptance criteria, test equipment calibration and control, procedural use

and compliance, control of temporary modifications or jumpers required for test

performance, documentation of test data, Technical Specification applicability, system

restoration, and evaluation of test data. Also, the inspectors verified that maintenance

and post-maintenance testing activities adequately ensured that the equipment met the

licensing basis, Technical Specifications, and Updated Safety Analysis Report (USAR)

design requirements.

b.

Findings

No findings of significance were identified.

1R22

Surveillance Testing (71111.22)

a.

Inspection Scope

The inspectors selected the following surveillance test activities for review. Activities

were selected based upon risk significance and the potential risk impact from an

unidentified deficiency or performance degradation that a system, structure, or

component could impose on the unit if the condition were left unresolved.

ECCS [Emergency Core Cooling System] Drywell Pressure Sensor Test (Week

Ending 7/27)

Drywell High Pressure Scram Test and Calibration (Week Ending 7/27)

Turbine Control Valve Fast Closure Scram Test and Calibration (Week

Ending 7/27)

Reactor Building to Torus Vacuum Breaker Operability Test (Week Ending 7/27)

12

GE 7700 Line Motor Control Center Maintenance Procedure (Week Ending 7/27)

Main Steam Isolation Instrument Test and Calibration (Week Ending 8/24)

Fire Protection Heat Actuated Detector Tests (Week Ending 9/21)

The inspectors observed the performance of surveillance testing activities, including

reviews for preconditioning, integration of testing activities, applicability of acceptance

criteria, test equipment calibration and control, procedural use, control of temporary

modifications or jumpers required for test performance, documentation of test data,

Technical Specification applicability, impact of testing relative to performance indicator

reporting, and evaluation of test data.

b.

Findings

No findings of significance were identified.

1R23

Temporary Plant Modifications (71111.23)

a.

Inspection Scope

The inspectors reviewed the following temporary modifications:

Drywell Equipment Drain Pump Bypass of Standby Function (Week Ending 9/28)

Disable of High Temperature Alarm for CRD-24-47 (Week Ending 10/5)

The inspectors reviewed the safety screening, design documents, USAR, and applicable

Technical Specifications to determine that the temporary modification was consistent with

modification documents, drawings and procedures. The inspectors also reviewed the

post-installation test results to confirm that tests were satisfactory and the actual impact

of the temporary modification on the permanent system and interfacing systems were

adequately verified.

b.

Findings

No findings of significance were identified.

1EP2

Alert and Notification System (ANS) Testing (71114.02)

a.

Inspection Scope

The inspectors discussed with emergency preparedness (EP) staff the design,

equipment, and periodic testing of the public ANS for the Monticello reactor facility

emergency planning zone to verify that the system was properly tested and maintained.

The inspectors also reviewed procedures and records for a 15 month period ending

June 2002, related to ANS testing, annual preventive maintenance, and non-scheduled

maintenance. The inspectors reviewed the licensees documentation for determining

whether each model of siren installed in the emergency planning zone would perform as

13

expected if fully activated. Records used to document and trend component failures for

each model of installed siren were also reviewed to ensure that corrective actions were

taken for test failures or system anomalies.

b.

Findings

No findings of significance were identified.

1EP3

Emergency Response Organization (ERO) Augmentation Testing (71114.03)

a.

Inspection Scope

The inspectors reviewed the licensees ERO augmentation testing to verify that the

licensee maintained and tested the ability to staff the ERO during an emergency in a

timely manner. Specifically, the inspectors reviewed quarterly, off-hours staff

augmentation test procedures, dated August 7, 2002, April 30, 2002, February 6, 2002,

November 1, 2001, August 7, 2001, May 8, 2001, February 8, 2001, November 14, 2000,

and August 7, 2000, test records, primary and backup provisions for off-hours notification

of the Monticello reactor facility emergency responders, and the current ERO rosters for

Monticello. The inspectors also reviewed and discussed the facility EP staffs provisions

for maintaining ERO call out lists.

b.

Findings

No findings of significance were identified.

1EP5

Correction of Emergency Preparedness Weaknesses and Deficiencies (71114.05)

a.

Inspection Scope

The inspectors reviewed the nuclear oversight staffs 2001 - 2002 audits and field

observations to ensure that these audits complied with the requirements of

10 CFR 50.54(t), and to ensure that the licensee adequately identified and corrected

deficiencies. The inspectors also reviewed the EP staffs 2002 self assessment and

critiques to evaluate the EP staffs efforts to identify and correct weaknesses and

deficiencies. Additionally, the inspectors reviewed a sample of EP items, condition

reports, and action requests related to the facilitys EP program to determine whether

corrective actions were acceptably completed.

b.

Findings

No findings of significance were identified.

14

1EP6

Drill Evaluation (71114.06)

a.

Inspection Scope

On September 4, 2002, the inspectors observed a simulator-based training evolution to

evaluate drill conduct and the adequacy of the licensees critique of performance to

identify weaknesses and deficiencies. The inspectors selected simulator scenarios that

the licensee had scheduled as providing input to the Drill/Exercise Performance Indicator.

The inspectors observed the classification of events, notifications to off-site agencies,

protective action recommendation development, and drill critiques. Observations were

compared to the licensees observations and corrective action program entries. The

inspectors verified that there were no discrepancies between observed performance and

performance indicator reported statistics. The simulator scenario observed resulted in an

alert classification.

b.

Findings

No findings of significance were identified.

2.

RADIATION SAFETY

Cornerstone: Occupational Radiation Safety

2OS1 Access Control

.1

Plant Walkdowns, Radiological Boundary Verifications, and Radiation Work Permit

Reviews (71121.01)

a.

Inspection Scope

The inspector conducted walkdowns of the radiologically restricted area to verify the

adequacy of radiological boundaries and postings. Specifically, the inspector walked

down several high and locked high radiation area boundaries in the reactor and turbine

buildings. The inspector observed the pre-job briefing and reviewed the radiation work

permit for main steam low pressure surveillance testing for protective clothing

requirements, dosimetry requirements including electronic dosimeter set points,

boundary controls, and radiation monitoring locations.

b.

Findings

No findings of significance were identified.

15

Cornerstone: Public Radiation Safety

2PS1

Radioactive Gaseous and Liquid Effluent Treatment and Monitoring Systems

.1

Offsite Dose Calculation Manual (ODCM) (71122.01)

a.

Inspection Scope

The inspector reviewed the 2001 Annual Radiological Environmental Operating Report to

verify that the radiological effluent program was implemented as described in the

Updated Safety Analysis Report (USAR) and the Offsite Dose Calculation Manual

(ODCM). The inspector reviewed the report for significant changes to the ODCM and to

the design and operation of the radioactive waste processing system. The inspector also

reviewed revisions made to the ODCM in calendar year 2001 and the justifications for the

changes, to verify they were completed and reported in accordance with Technical

Specifications and the ODCM.

b.

Findings

No findings of significance were identified.

.2

Gaseous and Liquid Release Systems Walkdowns (71122.01)

a.

Inspection Scope

The inspector performed walkdowns of selected components of the liquid and gaseous

effluent monitoring and control systems, including point of discharge effluent radiation

monitors to verify that the current system configuration was as described in the USAR

and was consistent with the ODCM, and to observe equipment material condition. The

inspector also discussed the gaseous waste processing system, including operations and

components with the cognizant system engineer.

b.

Findings

No findings of significance were identified.

.3

Gaseous and Liquid Releases (71122.01)

a.

Inspection Scope

The inspector reviewed liquid and gaseous radioactive waste (radwaste) release records

to verify that appropriate treatment equipment were used and that the radwaste effluents

were processed and released in accordance with the ODCM. As there were no liquid

batch releases performed during the inspection, the inspector reviewed the release

packages for two small unplanned liquid effluent releases made in 2001 and reported in

the 2001 Radioactive Effluent Release Report. The inspector reviewed the release

calculations to verify that the licensees release procedures and practices, including dose

projections to members of the public and use of station specific scaling factors, were

16

technically sound and conformed to ODCM methodology and Technical Specification

requirements. The inspector also reviewed selected gaseous effluent release data

including results of chemistry sample analyses, to independently verify that the data was

properly used to complete calculations of offsite dose. Additionally, the inspector

reviewed sample collection data to verify that compensatory samples were taken and

properly analyzed as required by the ODCM when the discharge canal water monitor was

out of service.

b.

Findings

No findings of significance were identified.

.4

Liquid and Gaseous Effluent Monitor Calibration

a.

Inspection Scope

The inspector reviewed records of instrument calibrations performed since the last

inspection for selected point of discharge effluent radiation monitors, to determine if they

had been calibrated consistent with industry standards and in accordance with station

procedures and the ODCM. Specifically, the inspector reviewed the calibration records

for:

Reactor Building Vent Wide Range Gas Monitor

Stack Wide Range Gas Monitor

Discharge Canal Monitor

Service Water Monitor

The inspector also reviewed current alarm setpoint values for these monitors to assess

compliance with ODCM requirements. Additionally, the inspector examined the

licensee's calendar year 2000 through 2001 data for tracking the reliability and

maintenance of selected point of discharge effluent radiation monitors, to assess the

adequacy of the licensee's efforts to identify repetitive problems and improve the overall

operating condition of the effluent radiation monitoring system.

b.

Findings

No findings of significance were identified.

.5

Dose Calculations (71122.01)

a.

Inspection Scope

The inspector reviewed the 2001 annual dose calculations and a selection of year

2002 monthly dose calculations to ensure that the licensee had properly calculated the

offsite dose to the public from radiological effluent releases, and to determine if any

17

annual Technical Specifications or ODCM (i.e., Appendix I to 10 CFR Part 50 values)

limits were exceeded.

b.

Findings

No findings of significance were identified.

.6

Air Cleaning Systems (71122.01)

a.

Inspection Scope

The inspector reviewed air cleaning system surveillance test results to ensure that test

results were within the licensees acceptance criteria. The inspector reviewed

surveillance test results for the station vent flow to verify that the flow rates were

consistent with USAR values.

b.

Findings

No findings of significance were identified.

.7

Counting Room Instrument Calibrations and Quality Control (71122.01)

a.

Inspection Scope

The inspector reviewed the quality control records for radiochemistry instrumentation

used to identify and quantify radioisotopes in effluents, to verify that the instrumentation

was calibrated and maintained as required by site procedures. This review included

calibrations of gamma spectroscopy systems.

b.

Findings

No findings of significance were identified.

.8

Interlaboratory Comparison Program (71122.01)

a.

Inspection Scope

The inspector reviewed the results of the 2001 Interlaboratory Comparison Program in

order to assess the quality of radioactive effluent sample analyses performed by the

licensee. The inspector reviewed the licensees quality control evaluation of the

interlaboratory comparison program and associated corrective actions for any

deficiencies identified.

b.

Findings

No findings of significance were identified.

18

.9

Identification and Resolution of Problems (71122.01)

a.

Inspection Scope

The inspector reviewed audits and self-assessments conducted during 2001 to evaluate

the effectiveness of the licensees self-assessment process in the identification,

characterization, and prioritization of problems. Selected condition reports written during

2000, 2001, and year to date 2002, that addressed radioactive treatment and monitoring

program deficiencies were also reviewed to verify that the licensee had effectively

implemented the corrective action program.

b.

Findings

No findings of significance were identified.

3.

SAFEGUARDS

Cornerstone: Physical Protection (PP)

3PP3

Response to Contingency Events (71130.03)

The Office of Homeland Security (OHS) developed a Homeland Security Advisory

System (HSAS) to disseminate information regarding the risk of terrorist attacks. The

HSAS implements five color-coded threat conditions with a description of corresponding

actions at each level. USNRC Regulatory Issue Summary (RIS) 2002-12a, dated

August 19, 2002, NRC Threat Advisory and Protective Measures System, discusses the

HSAS and provides additional information on protective measures to licensees.

a.

Inspection Scope

On September 10, 2002, the USNRC issued a Safeguards Advisory to reactor licensees

to implement the protective measures described in RIS 2002-12a in response to the

Federal government declaration of threat level "Orange." Subsequently, on

September 24, 2002, the OHS downgraded the national security threat condition to

"Yellow" and a corresponding reduction in the risk of a terrorist threat.

The inspectors interviewed licensee personnel and security staff, observed the conduct

of security operations, and assessed licensee implementation of the threat level

"Orange" protective measures. Inspection results were communicated to regional and

headquarters security staff for further evaluation.

b.

Findings

No findings of significance were identified.

19

4.

OTHER ACTIVITIES

4OA1 Performance Indicator (PI) Verification (71151)

Cornerstones: Mitigating Systems, Barrier Integrity, and Emergency Preparedness

.1

Mitigating Systems and Barrier Integrity Performance Indicator Verification

a.

Inspection Scope

During the week ending July 27, 2002, the inspectors reviewed licensee event reports

(LERs), licensee memoranda, plant logs, and prior USNRC inspection reports to verify

the following performance indicators for the 3rd quarter of 2002:

Safety System Functional Failures

Reactor Coolant System Specific Activity

b.

Findings

No findings of significance were identified.

.2

Emergency Preparedness Performance Indicator Verification

a.

Inspection Scope

The inspector verified that the licensee had accurately reported the following

performance indicators:

ANS

ERO Drill Participation

Drill and Exercise Performance (DEP)

Specifically, the inspector reviewed the licensees PI records, data reported to the

USNRC, and condition reports for the period April 2001 through June 2002 to identify any

occurrences that were not identified by the licensee. Records of relevant control room

simulator training sessions, periodic ANS tests, and excerpts of drill and exercise

scenario and evaluations were also reviewed.

b.

Findings

No findings of significance were identified.

20

.3

Data Submission Issue

a.

Inspection Scope

During the week ending July 27, 2002, the inspectors reviewed the data submitted by the

licensee for the 3rd quarter 2002 performance indicators for any inconsistencies prior to

its public release in accordance with IMC 0608, "Performance Indicator Program."

b.

Findings

No findings of significance were identified.

4OA3 Event Follow-up (71153)

Cornerstone: Barrier Integrity

.1

(Closed) Licensee Event Report (LER) 50-263/2002-004: Unplanned Loss of Both

Trains of Control Room Ventilation During Auto Start Testing Due to Timing Circuit Relay

Failure

On April 1, 2002, both trains of the control room ventilation system (CRV) were found to

be inoperable during routine surveillance testing. During performance of the test, Train B

of CRV is made inoperable to induce a low flow signal and validate the auto start feature

of Train A. Upon performance of the test CRV Train A failed to auto start, thereby

causing both trains of CRV to be simultaneously inoperable. Upon discovery,

appropriate Technical Specifications were entered and all conditions of the license met.

The inspectors reviewed the issue and determined the safety significance to be very low

because, with the exception of the performance of the test, both the Train B auto start

feature and the Train A manual initiation feature were always operable. The licensee has

entered this issue into their corrective action program as Condition Report

(CR) 20023185.

4OA4 Cross-cutting Issues

Human Performance

A finding of very low safety significance (Green) and an associated NCV for failure to

follow applicable procedural guidance were identified by inspectors. The finding and

NCV were associated with a loss of spent fuel pool cooling which resulted from an

improper licensee valve tagout/clearance operation. The cause of the improper valve

tagout/clearance operation was the system engineers and licensed operators lack of

understanding of the system and their failure to adhere to the cautions in the system

operating procedure. A contributing cause was a less than complete turnover from the

previous system engineer. The errors involved were determined to be human

performance related. (Section 1R13)

21

4OA6 Meetings

.1

Exit Meeting

The inspectors presented the inspection results to Mr. J. Purkis and other members of

licensee management on October 3, 2002. The licensee acknowledged the findings

presented. The inspectors asked the licensee whether any materials examined during

the inspection should be considered proprietary. No proprietary information was

identified.

.2

Interim Exit Meetings

Interim exit meetings were conducted for:

Emergency Preparedness Inspections with Mr. J. Purkis on August 16, 2002

Radiation Protection Inspections with Mr. J. Purkis on August 23, 2002

22

KEY POINTS OF CONTACT

Licensee

R. Baumer, Licensing

G. Bregg, Manager, Quality Services

G. Brevig, Internal Assessment Supervisor

T. Corrigan, Radiation Protection Technician

D. Fadel, Director of Engineering

J. Forbes, Site Vice-President

J. Grubb, General Superintendent, Operations

M. Holmes, Chemistry Supervisor

G. Holthaus, Emergency Preparedness Coordinator

D. Horgen, Emergency Preparedness Instructor

K. Jepson, General Superintendent, Chemistry and Radiation Services

B. Linde, Superintendent, Security

D. Neve, Licensing Project Manager

D. Pedersen, Acting Emergency Preparedness Manager

J. Purkis, Plant Manager

B. Sawatzke, General Superintendent, Maintenance

C. Schibonski, General Superintendent, Safety Assessment

E. Sopkin, General Superintendent, Engineering

A. Ward, Business Support Manager

L. Wilkerson, Operations Support

USNRC

B. Burgess, Chief, Reactor Projects Branch 2

23

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

Opened

50-263/02-05-01

NCV

Tagout/Isolation Error Discharges 2000 Gallons From Fuel Pool

Surge Tank To Radwaste and Results in Loss of Spent Fuel Pool

Cooling (Sections 1R13 and 4OA4)

Closed

50-263/02-05-01

NCV

Tagout/Isolation Error Discharges 2000 Gallons From Fuel Pool

Surge Tank To Radwaste and Results in Loss of Spent Fuel Pool

Cooling (Sections 1R13 and 4OA4)

50-263/2002-004

LER

Unplanned Loss of Both Trains of Control Room Ventilation

During Auto Start Testing Due to Timing Circuit Relay Failure

(Section 4OA3.1)

Discussed

None.

24

LIST OF ACRONYMS USED

AC

Alternating Current

ANS

Alert and Notification System

ASME

American Society of Mechanical Engineers

ATWS

Anticipated Transient Without Scram

AWI

Administrative Work Instruction

CAM

Continuous Air Monitor

CFR

Code of Federal Requirements

CR

Condition Report

CRD

Control Rod Drive

CRV

Control Room Ventilation

DBD

Design Basis Document

DC

Direct Current

DEP

Drill and Exercise Performance

DRP

Division of Reactor Projects

DW

Drywell

DWEDS

Drywell Equipment Drain Sump

ECCS

Emergency Core Cooling System

EDG

Emergency Diesel Generator

EFT

Emergency Filtration Train

EMD

Electromotive Division

EP

Emergency Preparedness

EPR

Electronic Pressure Regulator

FOI

Follow-On Item

HPCI

High Pressure Core Injection

HSAS

Homeland Security Advisory System

IMC

Inspection Manual Chapter

IPEEE

Individual Plant Examination of External Events

IR

Inspection Report

LCO

Limiting Condition For Operation

LER

Licensee Event Report

LPCI

Low Pressure Core Injection

MCC

Motor Control Center

NCV

Non-Cited Violation

NEI

Nuclear Energy Institute

NMC

Nuclear Management Company

NUMARC

Nuclear Management and Resources Council

ODCM

Offsite Dose Calculation Manual

OHS

Office of Homeland Security

OWI

Operations Work Instruction

P&ID

Piping and Instrumentation Drawing

PANS

Public Alert Notification System

PI

Performance Indicator

RBV

Reactor Building Ventilation

RCIC

Reactor Core Isolation Cooling

RCS

Reactor Coolant System

RFO

Refueling Outage

25

RHR

Residual Heat Removal

RHRSW

Residual Heat Removal Service Water

RIS

Regulatory Issue Summary

RP

Radiation Protection

RPS

Radiation Protection Specialist

SCTMT

Secondary Containment

SDP

Significance Determination Process

SER

Safety Evaluation Report

SRI

Safety Review Item

TS

Technical Specification

USAR

Updated Safety Analysis Report

USNRC

U.S. Nuclear Regulatory Commission

26

LIST OF DOCUMENTS REVIEWED

1R04

Equipment Alignment

NF-36298-1

Electrical Load Flow One Line Diagram

Revision P

B.9.13

Instrument AC and Uninterruptible AC

Distribution System

NH-36251

P&ID RCIC (Steam Side) Diagram

Revision AN

NH-36252

P&ID RCIC (Water Side) Diagram

Revision AC

B.02.03-01

Reactor Core Isolation Cooling Functional and

General Description of System

November 3, 2000

B.02.03-02

Reactor Core Isolation Cooling Description of

Equipment

December 15, 2000

B.02.03-03

Reactor Core Isolation Cooling Instrumentation

and Controls

November 3, 2000

B.02.03-05

Reactor Core Isolation Cooling System Operation

June 24, 2002

CR 20011367

Drain Line Configuration for RCIC 50 As-shown

does not match As-Built

March 8, 2001

CR 20011420

Potential to Pressurize HPCI and RCIC Suction

Piping Above Design Not Recognized in Check

Valve Cold S/V Tests

March 9, 2001

CR 20012898

Failed PMT per WO 0107737 Results in RCIC

Inoperability for Additional 4 hours4.62963e-5 days <br />0.00111 hours <br />6.613757e-6 weeks <br />1.522e-6 months <br />

May 25, 2001

CR 20014637

Basis For RCIC Cooling Water Flow

Requirement Cannot Be Located

September 11, 2001

CR 20016336

Declared RCIC Inoperable and Entered

Unplanned LCO Due to Indicated Turbine Inlet

Drain Pot High Level

October 20, 2001

CR 20021666

Drawing Discrepancies Noted on Three RCIC

Drawings

February 22, 2002

CR 20024414

MO-2076 Failed to Fully Open During RCIC

Steam Line High Area Temperature Test and

Calibration

May 8, 2002

CR 20025729

Final Results of RCIC Design Self Assessment

June 21, 2002

CR 20025730

Declining Trend of RCIC NRC Indicators for

Several Quarters

June 21, 2002

27

CR 20026529

RCIC-65 was Physically Moved During RFO

2001 and Champs was Not Updated

July 16, 2002

M-121

Residual Heat Removal System (Division I)

Revision BM

2120

Plant Prestart Checklist RHR System

Revision 8

2154-12

Residual Heat Removal System Prestart Valve

Checklist

Revision 35

B.3.4

Operations Manual: Residual Heat Removal

System

Revision 4

Section 6.2

USAR:

- Emergency Core Cooling Systems

Revision 19

M-120

Residual Heat Removal System (Division II)

Revision BJ

1R05

Fire Protection

NX-16991

Technical Manual, Monticello Updated Fire

Hazards Analysis

A.3-13A

A.3-13B

A.3-13C

A.3-15B

A.3-18A

A.3-18B

A.3-20

A.3-21

A.3-04D

Pre-Fire Strategies:

- Lube Oil Storage Tank Room

- Reactor Feedpump and Lube Oil Reservoir

Room

- Turbine Building 911 Elevation East MCC Area

- No. 11 Diesel Generator Room and Day Tank

Rooms

- Hot Machine Shop

- Oil Drum Storage Room

- Auxiliary Boiler Room

- Radwaste Shipping Building

- Standby Gas Treatment Room

Revision 3

Revision 5

Revision 2*

Revision 6

Revision 3

Revision 2

Revision 4

Revision 3

Revision 3*

A.2-101

2176

Drill Guide No. 15

5790-103-01

Procedures and Forms:

- Classification of Emergencies

- Fire Drill Procedure

- Fire at MCC 133 and Reactor Feed Pump Area

- Alert Checklist

Revision 28

Revision 12

Revision 11

1R06

Flood Protection Measures

DBD - T.5

Design Basis Document (DBD) T.5, External

Flooding

28

91-0126

91-0125

91-0073

Design Basis Document Follow-On Items (FOI):

- Emergency Procedure A.6, Section B

(Flooding) Concerns

- Unlocated External Flood Study Documents

- Predicted Delivery Time for Sandbags

Individual Plant Examination of External Events

(IPEEE)

Section 12.2.1.7.1

Section 2.4.1

Section 1.3.1.4

Updated Safety Analysis Report (USAR):

- External Flooding

- Surface Water

- Hydrology

Revision 19

M-801

M-803

M-804

M-805

Intake Structure Drawings

A.6

Operations Manual:

- External Flooding

Revision 0

NH-178639

Flood Barriers for A.6 Acts of Nature Procedure

Revision A

NH-33453

Intake Structure Sections and Detail - Sheet 1

Revision A

NF-36454

Intake Structure Plan at Elevation 919-0"

Revision D

MNTS-83-0438

Flood Protection Requirements for Maximum

Probable Flood, 82-02-SPEC

FOI 96-0116

Qualification of the Intake Structure Pump Room

Slab and Hatches Due to Probable Maximum

Flood Uplift Pressure Loads

3/11/93

1R11

Licensed Operator Requalification Program

RQ-SS-08E

Simulator Exercise Guide - Spurious Group 1

With an ATWS

Revision 6

B.03.05-05.G.1

Standby Liquid Control System

Revision 9

C.4-G

Inadvertent ECCS Initiation

Revision 2

C.5-3101

Alternate Rod Insertion

Revision 3

C.5.3205

Terminate and Prevent Injection

Revision 2

29

1R12

Maintenance Effectiveness

93-01

93-01, Section 11

NUMARC [Nuclear Management and Resources

Council]:

- Nuclear Energy Institute Industry Guideline for

Monitoring the Effectiveness of Maintenance at

Nuclear Power Plants

- Assessment of Risk Resulting from the

Performance of Maintenance Activities

Revision 2

February 22, 2000

1.160

1.182

Regulatory Guides:

- Monitoring the Effectiveness of Maintenance at

Nuclear Power Plants

- Assessing and Managing Risk Before

Maintenance Activities at Nuclear Power Plants

Revision 2

May 2000

05.02.01

Engineering Work Instruction, Monticello

Maintenance Rule Program Document

Revision 5

B.8.4.1

Operations Manual:

- Instrument and Service Air

B.8.4.1

Maintenance Rule Program System Basis

Document:

- Instrument and Service Air

Revision 2

10.3.4

USAR:

- Plant Air Systems and Nitrogen Systems

Revision 19

WO 0203880

Install Temp Air Compressor To Supply

Discharge Structure

3278

NMC Standard 10 CFR 50.59 Screening Form -

Screening Number SCR-02-0462, Revision 0

Revision 3*

3434

Jumper Bypass Form, Dated 8/2/02, for

Temporary Instrument Air System WO 0203880

Revision 20

Maintenance Rule Performance Data for

Instrument Air System

January 2000 to

August 8, 2002

CR 20017166

13 Air Compressor Tripped on Low Lube Oil

Pressure Due to Cool Ambient Conditions

WO 0203873

May Be Air Leaking-Bubbling in Puddle North of

E-100A

CR 20027014

Air Leaking up From Ground by East Side of

Cooling Tower

M-131

Piping and Instrument Diagram, Instrument Air -

Turbine Building

Revision AA

30

M-800-1

Piping and Instrument Diagram, Circulating

Water System

Revision A

1R13

Maintenance Risk Assessments and Emergent Work Control

4AWI-04.01.01

SWI-14.01

Procedures:

- General Plant Operating Activities

- Risk Management of On-line Maintenance

Revision 33

Revision 0

M-131

M-136

M-135

Drawings and Prints:

- Instrument Air - Turbine Building

- Fuel Pool Filter/Demin

- Fuel Pool Cooling and Clean Up System

Revision AA

Revision T

Revision AB

CR 20027014

Air Leak Bubbling up from Ground by East Side

Cooling Tower

WO 0203987

CRD Pump Casing Bolt to Casing Leak

Reactor and Control Room Log

August 23, 2002

B.2.1-05

Operations Manual:

- Fuel Pool Cooling System Operation

Revision 14

1R15

Operability Evaluations

CR 20026336

12 EDG Lube Oil Lead Content Increasing to

Point of Additional Monitoring

MI 1760

Lubricating Oil for EMD Engines - Marine, Power,

and Drilling Rig

Revision G

MI 1762

Lubricating Oil for Industrial Power Engines

Revision E

MI 1750

Diesel Fuel Recommendations All EMD and

Former COED Engines

Revision H

TRF 90-215

Product Data Sheet - Mobilgard 450

CR 20026579

Main Steam Line Radiation Monitors Not

Maintained with Safety-Related Parts

Section 7.5

USAR:

- Plant Radiation Monitoring System

Revision 19

B.05.11

Operations Manual:

- Process Radiation Monitoring System

TAC No. M82783

License Amendment No. 83

August 18, 1992

CR 20027876

Flanged Connection Bolting for FP-13 (Diesel

Fire Pump Check Valve) Has Insufficient Thread

Engagement

31

EPRI TR-104213s

Electric Power Research Institute Report - Bolted

Joint Maintenance & Application Guide

December 1995

CR 20027020

RHR Corner Room Calculation Assumptions Are

Inconsistent with Current Plant Operating

Practices

CR 20027443

Running Room Coolers for the RHR Rooms

Continuously Could Be a Concern in the Winter

CR 20026989

SRI 86-015 Allowed a 2 Hour Operation with No

RHR Room Cooling Inconsistent with Heatup

Calc CA 97-157 Rev 1 Assumptions

1R16

Operator Workarounds

C.6-007-B-17

C.4-B.6.3.A

Operations Manual:

- Alarm Response For 24" Vacuum Trip No. 2

- Decreasing Condenser Vacuum

Revision 1

Revision 7

OWI-01.07

Operations Work Instruction:

- Operations Department Self Assessment

Revision 17

CR 20025993

Unexpected Alarm C07-B-17, Vacuum 24 Inch

Trip No. 2

1R17

Permanent Plant Modifications

CR 20027798

American Air Filter Replacement Charcoal Trays

Do Not Match Currently Installed Trays

02A047

Alteration Package - Replacement of Charcoal

Filter Trays in the EFT System

August 20, 2002

NEI 96-07

Guidelines For 10 CFR 50.59 Implementation

Revision 1

4AWI-06.01.05

4AWI-05.06.02

Procedures:

- Alteration Process

- 10 CFR 50.59 Applicability and Screening

Revision 11

Revision 5

32

1R19

Post-Maintenance Testing

0255-08-IA-1

3069

3069

0255-06-IA-1

1158-B

4190-OCD

4058-03

Procedures and Forms:

- RCIC System Pump Flow and Valve Tests

- Post-Maintenance Testing Activities Control

Cover Sheet for WO 0204052

- Post-Maintenance Testing Activities Control

Cover Sheet for WO 0200757

- HPCI Pump Flow and Valve Tests

- Diesel Fire Pump Weekly Check

- Diesel Engine, Fire Protection Pump

- RHRSW Pump No. 11 and No. 13 Motor Cooler

Chemical Cleaning and Pressure Test

Revision 51

Revision 11

Revision 11

Revision 58

Revision 12

Revision 13

Revision 7

WO 0203204

No. 12 EDG Testing Following Speed Changing

Motor Replacement/Repair

WO 0110563

PI-13-69 Isolation Valve Packing Leak

WO 0110650

Small Leak Through Plug on RCIC Trip Valve

MO-2080 on PS-13-72B

WO 0204123

Replace Diesel Fire Pump Coolant Hose

WO 0204052

Repair of CV-3503 Air Line

CR 20027611

Air Line Failed on HPCI Test Return Valve

CV-3503 Resulting In Aborted Test and Extended

HPCI LCO Time. WO Initiated

B.08.05

Operations Manual:

- Fire Protection

Section 10.3.1

USAR:

- Fire Protection System

Revision 19

33

1R22

Surveillance Testing

0030

0003

0011-A

0141

4847-PM

0054-B

Procedures and Forms:

- ECCS Drywell Pressure Sensor Test

- Drywell High Pressure Scram and Group 2, 3

and SCTMT Isolation Test and Calibration

- Turbine Control Valve Fast Closure SCRAM

Test and Calibration (>30% of Rated)

- Reactor Building to Torus Vacuum Breaker

Operability Test

- GE 7700 Line Motor Control Center

Maintenance Operability Test

- Main Steam Line Low Pressure Group 1

Isolation Instrument Test and Calibration

(Reactor in Run)

Revision 10

Revision 16

Revision 3

Revision 19

Revision 11

Revision 5

3.2/4.2

Technical Specifications:

- Protective Instrumentation

PS-10-101A-D

Instrument Calibration Worksheet

July 15, 2002

WO 0204394

Perform Intake Structure Pre-Action Detector

Test

WO 0204393

Perform Diesel Pre-Action Detector Test

NFPA 72E-1974

Chapter 7: Maintenance and Testing

NFPA 72E-1982

Chapter 8: Maintenance and Testing

1R23

Temporary Plant Modifications

3034

Jumper Bypass 02-39, Prevent Starting of P-20A

When Moving Switch Through Standby Position

Revision 20

3034

Jumper Bypass 02-40, Disable of High

Temperature Alarm for CRD-24-47 From

TR-3-244 by Program Change

Revision 20

WO 0204379

Spurious CRD High Temp Alarm TR-3-244

1EP2

Alert and Notification System (ANS) Testing

Monticello Area PANS Implementing Procedure

and Supplementary Documents

June 1, 1984

NF-108565-2

Monticello Emer. Plan Sirens and Contours

May 15, 1999

Project 01Q095

Public Alert Notification System Replacement

Revision 0

Surv. Test 1359

PANS Weekly Cancel Signal Test

Revision 6

Surv. Test 1409

PANS Monthly Siren Activation Testing

Revisions 3-7

Contract

Agreement

MNGP Public Alert and Notification System

October 22, 1996

34

General Conditions For Maintenance, Repair,

And Operations Contracts

September 24, 1996

PANS Monthly Test Report, Failure Matrix

February-May 2002

FEMA Letter

MNGP Alert and Notification System Evaluation

April 25, 1985

EPWI-01.05

PANS Maintenance And Testing

Revision 0

1EP3

Emergency Response Organization (ERO) Augmentation Testing

Sections 5.0 & 7.0

MNGP Emergency Plan

Revision 21

5790-001-01

MNGP Emergency Response Organization

August 6, 2002

Surv. Test 1317

MNGP Emergency Alert Notification System Test

Revision 12

5790-104-04

Emergency Call List-Alert/Site Area/General

June 5, 2002

Surv. Test 1317

MNGP Emergency Alert Notification System Test

Results: August 2000 - August 2002

1EP5

Correction of Emergency Preparedness Weaknesses and Deficiencies

Nuclear Oversight 1st Quarter 2002 Assessment

Report For Monticello

April 30, 2002

2002-001-5-002

Nuclear Oversight Observation Report

April 3, 2002

2002-001-5-046

Nuclear Oversight Observation Report

April 24, 2002

Self Assessment

Emergency Preparedness Program Assessment

August 9, 2002

AG 2001-S-1

Internal Audit Report, Emergency Preparedness

April 30, 2001

AG 2000-S-1

Internal Audit Report, Emergency Preparedness

April 28, 2000

4AWI-10.01.03

Condition Report Process

Revision 18

Drill Critique Report Conducted April 25, 2001

Exercise Critique Report Conducted June 6,2001

Drill Critique Report Conducted March 27, 2002

Drill Critique Report Conducted June 12, 2002

CA 20003000

Add SER Lessons Learned To EP Training

August 3, 2000

CA 20003370

Provide Ops. Shift Mgt. Guidance On Filling

Unexpected Vacancies

September 6, 2000

CA 20010988

Evaluate Need For Training Shift Em. Comms.

February 20, 2001

CR 20015705

Discrepancies Noted In Em. Equip. Inventory

September 27, 2001

CR 20020316

PASS Procedures Were Wrong Revisions

January 17, 2002

CR 20020362

Em. Plan Proc. Manual Found With Old Revision

January 18, 2002

CR 20020369

Em. Equip. Locker Has Old Revisions EP Maps

January 18, 2002

CR 20020374

Em. Plan Manual Missing Some Procedures

January 18, 2002

CR 20023651

Corrective Actions To Resolve EP Inventory

Problems

April 17, 2002

CR 20024480

NOUE Classification Review (Ft. Calhoun)

May 10, 2002

CR 20023409

Evacuation From The Owner Controlled Area

August 2, 2002

CR 20016978

ERO Augmentation Test Issues

November 7, 2001

CR 20010175

Re-evaluation Of Policy On KI

March 9, 2001

35

CR 20012400

Assessment Of April 25, 2001 Full Scale Drill

July, 23, 2001

CR 20013176

Critique Of June 6, 2001, EP Exercise

August 14, 2001

CR 20014820

Less Than 30% ERO Respond For Pager Test

August 14, 2001

CR 20003136

Inadvertent Activation Of PANS For Weekly Test

August 17, 2000

CR 20026555

EP Inventory Surveillance Finds Missing Items

July 17, 2002

CR 20025894

PANS Electrical Disconnect Notice Received

June 27, 2002

CR 20016589

Abnormal Procedure Issued Without EP 50.54(q)

October 30, 2001

CR 20014819

Failure To Meet Min. Staffing During ERO Test

August 14, 2001

CR 20015043

Failure To Identify Default PAR In Simulator

August 27, 2001

1EP6

Drill Evaluation

A.2-101

5790-103-01

5790-102-02

5790-501-03

5790-104-04

Procedures and Forms:

- Classification of Emergencies

- Alert Checklist

- Emergency Notification Report Form

- Emergency Communicator Checklist

- Emergency Call List - Alert/Site Area/General

Revision 28

Revision 11

Revision 25

Revision 4

Revision 77

RQ-SS-08E

Simulator Exercise Guide - Spurious Group 1

With an ATWS

Revision 6

2PS1

Radiological Effluents

0147

Standby Gas Treatment System Filter Tests

Revision 10

0149

Standby Gas Treatment Charcoal Adsorber

Cartridge Test

Revision 7

0163

Stack Wide Range Gas Monitor Calibration

Revision 25

0171

Discharge Canal Monitor Calibration

Revision 13

0248

Reactor Building Vent Wide Range Gas Monitor

Calibration

Revision 21

0290

Service Water Monitor Calibration

Revision 8

0363-01

RBV Wide Range Gas Monitors Process and

Sample Flow Instrument Calibration Procedure

Revision 5

0372

Stack Wide Range Gas Monitors Process and

Sample Flow Instrument Calibration Procedure

Revision 8

0385-A

Drywell Particulate Monitor Functional Test

Revision 8

1118

Off-Gas Compressors Suction Filters DOP and

Freon Efficiency Test

Revision 5

1119

Stack Filters DOP Efficiency Test

Revision 3

36

1399

Liquid Process Monitor-Grab Sampling

Revision 3

5090

Software Verification-Liquidose

Revision 3

CR 20027821

Improper Routing of Drain Hose Results in

Unplanned Radioactive Liquid Release

December 4, 2001

CR 20020231

2001 Chemistry Self-Assessment

January 16, 2002

CR 20022866

Discharge Canal Monitors Experience a MRFF Due

to Loss of SX Pump During Storm

March 22, 2002

CR 20023425

Received Discharge Canal Hi Radiation Alarm 4-B-22

April 10, 2002

CR 20024422

Discharge Canal Hi Rad, 4-A-22 was Received

Following Heavy Rain

May 8, 2002

CR 20025368

Received Discharge Canal Hi Rad Alarm 4-A-22

During Period of Heavy Rain

June 7, 2002

CR 20026685

Discharge Canal Hi Rad 4-A-22 Received Following

Heavy Rain

July 20, 2002

CR 20026950

Received Discharge Canal High Radiation Alarm 4-B-22

July 29, 2002

CR 20027107

Annunciator 4-A-22 Discharge Canal Hi Radiation

Alarms whenever Heavy Rains Occur. Operational

Challenge 02-048

August 1, 2002

Abnormal-Release Calculations Week #52 of 2001

December 4, 2001

Section 9.3

USAR: Plant Radioactive Waste Control Systems

Revision 19

2001 Radioactive Effluent Release Report

May 15, 2002

Internal Correspondence-Revision to ODCM

November 30, 2000

4OA1 Performance Indicator Verification

Monticello Performance Indicator Data Summary

Report - 2nd Quarter 2002

July 3, 2002

NEI 99-02

Regulatory Assessment Performance Indicator

Guideline

Revision 2

3530-09

NRC Performance Indicator Safety System

Functional Failures

Revision 2

3530-08

Performance Indicator RCS Activity Worksheet

Revision 2

1.3.13

Reactor Water and Cleanup Systems Iodine

Revision 11

37

CR 20014093

Unexpected Alarm DW Equipment Drain Leak

Rate During Pump Down of DWEDS

July 12, 2001

CR 20014636

Unexpected Alarm 3-A-17 Auto Blowdown Valve

Bellows Leaking

August 3, 2001

CR 20014975

Tiny Leak in HPCI Main Pump

August 22, 2001

CR 20015261

Unexpected Alarm C04-B-13 Drywell Equipment

Drain Leak Rate High

September 8, 2001

CR 20016595

Unexpected Alarm C04-B-13 Drywell Equipment

Drain Leak Rate High

October 31, 2001

CR 20018193

Leakage Observed from RV-2031 After

Completion of RHR Surveillance

December 20, 2001

CR 20020010

Received Annunciator C-04-B-13 Drywell

Equipment Drain Leak Rate High

January 2, 2002

CR 20020078

Unexpected Alarm C04-B-13 Drywell Equipment

Drain Leak Rate High

January 5, 2002

CR 20022008

Unexpected Alarm C04-B-13 Drywell Equipment

Drain Leak Rate High

March 1, 2002

CR 20022737

Unexpected Alarm C04-B-13 Drywell Equipment

Drain Leak Rate High

March 19, 2002

CR 20023139

Packing Leak on HWC-61-1 Degraded Steam

Leak

March 29, 2002

CR 20024350

Unexpected Alarm C04-B-13 Drywell Equipment

Drain Leak Rate High when P-20 Started

May 6, 2002

CR 20025147

Small Steam Leak from HPCI Instrument Root

Valve R-6

June 2, 2002

CR 20025262

DW CAM Count Rate Increasing with

Corresponding Increase in DW Floor Drain

Leakage

June 4, 2002

CR 20025527

Received Alarm 4-B-32 DWEDS High

Temperature and 4-B-18 DWEDS Leak Rate

Change High Simultaneously

June 14, 2002

CR 20025986

Unexpected Alarm C04-B-13 Drywell Equipment

Drain Leak Rate High

June 30, 2002

CR 20026217

Unexpected Alarm C04-B-13 Drywell Equipment

Drain Leak Rate High

July 5, 2002

EPWI-01-06

Emergency Plan Performance Indicator Program

Revision 0

38

PANS Quarterly Operability Results: April 2001 -

June 2002

ERO Quarterly Participation Results: April 2001 -

June 2002

DEP Quarterly Performance Results: April 2001

- June 2002

4OA3 Event Follow-up

LER 2002-004

Unplanned Loss of Both Trains of Control Room

Ventilation During Auto Start Testing Due to

Timing Circuit Relay Failure

Revision 0

CR 20023185

Entered Unplanned 24 Hour LCO Upon Failure of

V-EAC-14A to Auto Start on Low Flow per

CRV-EFT Test 1429

WO 0201969

Investigate/Repair V-EAC-14A Auto Start Relay

Circuitry

CR 20023386

Revise Procedure 1429 to Correct LCO Entries.

Attempt to Develop Test Method Which Will Not

Create 24-hour LCO Entry

1429

CRV-EFT Low Flow Test

Revision 10

CR 20023387

Submit a Request for Estimate on Replacing

Struthers / Dunn Relays With Alt Control System

to the Plant Health Committee