ML022750524

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IR 05000346-02-008, on 05/15-08/09/2002, Firstenergy Nuclear Operating Company, Davis-Besse Nuclear Power Station. Augmented Inspection Team Follow-up Special Inspection
ML022750524
Person / Time
Site: Davis Besse 
Issue date: 10/02/2002
From: Grobe J
NRC/RGN-III
To: Myers L
FirstEnergy Nuclear Operating Co
References
FOIA/PA-2005-0261 IR-02-008
Download: ML022750524 (36)


See also: IR 05000346/2002008

Text

October 2, 2002

Mr. Lew W. Myers

Chief Operating Officer

FirstEnergy Nuclear Operating Company

Davis-Besse Nuclear Power Station

5501 North State Route 2

Oak Harbor, OH 43449-9760

SUBJECT:

DAVIS-BESSE NUCLEAR POWER STATION

NRC AUGMENTED INSPECTION TEAM FOLLOW-UP SPECIAL

INSPECTION REPORT NO. 50-346/02-08(DRS)

Dear Mr. Myers:

On March 12, 2002, the USNRC dispatched an Augmented Inspection Team (AIT) to the

Davis-Besse site in accordance with USNRC Management Directive 8.3, USNRC Incident

Investigation Program. The AIT was chartered to determine the facts and circumstances

related to the significant degradation of the reactor vessel head pressure boundary material.

The AIT developed a sequence of events, interviewed plant personnel, collected and analyzed

factual information relevant to the degraded condition and conducted visual inspections of the

reactor vessel head. The AIT results were summarized for you and your staff during a public

exit meeting on April 5, 2002, and the AIT report was issued on May 3, 2002.

On May 15, 2002, USNRC began a special inspection focused on compliance with USNRC

rules and regulations as they relate to the facts and circumstances associated with the

degradation of the reactor pressure vessel head documented in the AIT report. On August 9,

2002, the USNRC completed this special inspection. The enclosed report documents the

inspection findings which were discussed with you and other members of your staff on August

9, 2002.

Based on this special inspection, ten findings, some apparent violations with multiple examples,

were identified and are documented in the enclosed report. Those findings include: operating

the reactor with prohibited pressure boundary leakage; failure to take effective action to correct

multiple identified safety concerns; inadequacies in the boric acid corrosion control procedure;

failure to effectively implement the boric acid corrosion control procedure and the corrective

action procedure; and multiple examples of inaccurate or incomplete information in letters to the

USNRC or records required by the USNRC to be maintained onsite. Because the USNRCs

determination of the safety significance of the reactor vessel head degradation has not been

finalized and several of these apparent violations remain under review by the USNRC, all of

these findings are currently characterized as unresolved items in the enclosed report.

L. Myers

-2-

In accordance with 10 CFR Part 2.790 of the USNRC's Rules of Practice, a copy of this letter

and its enclosure will be available electronically for public inspection in the USNRC Public

Document Room or from the Publicly Available Records (PARS) component of USNRC's

document system (ADAMS). ADAMS is accessible from the USNRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

John A. Grobe, Chairman

Davis-Besse Oversight Panel

Docket No.

50-346

License No.

NPF-3

Enclosure:

USNRC Inspection Report

No. 50-346/02-08(DRS)

cc w/encl:

B. Saunders, President - FENOC

Plant Manager

Manager - Regulatory Affairs

M. OReilly, FirstEnergy

Ohio State Liaison Officer

R. Owen, Ohio Department of Health

Public Utilities Commission of Ohio

President, Board of County Commissioners

Of Lucas County

President, Ottawa County Board of Commissioners

D. Lochbaum, Union of Concerned Scientists

L. Myers

-2-

In accordance with 10 CFR Part 2.790 of the USNRC's Rules of Practice, a copy of this letter

and its enclosure will be available electronically for public inspection in the USNRC Public

Document Room or from the Publicly Available Records (PARS) component of USNRC's

document system (ADAMS). ADAMS is accessible from the USNRC Web site at

http://www.nrc.gov/reading-rm/adams.html (the Public Electronic Reading Room).

Sincerely,

/RA/

John A. Grobe, Chairman

Davis-Besse Oversight Panel

Docket No.

50-346

License No.

NPF

Enclosure:

USNRC Inspection Report

No. 50-346/02-08(DRS)

cc w/encl:

B. Saunders, President - FENOC

Plant Manager

Manager - Regulatory Affairs

M. OReilly, FirstEnergy

Ohio State Liaison Officer

R. Owen, Ohio Department of Health

Public Utilities Commission of Ohio

President, Board of County Commissioners

Of Lucas County

President, Ottawa County Board of Commissioners

D. Lochbaum, Union of Concerned Scientists

DOCUMENT NAME: G:DRS\\ML022750524.wpd

To receive a copy of this document, indicate in the box: "C" = Copy without attachment/enclosure "E" = Copy with attachment/enclosure "N" = No copy

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ADAMS Distribution:

Chairman Meserve

Commissioner Dicus

Commissioner Diaz

Commissioner McGaffigan

Commissioner Merrifield

W. Travers, EDO

W. Kane, OEDO

S. Rosenberg, OEDO

B. Bonser, OEDO

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S. Collins, NRR

B. Sheron, NRR

J. Zwolinski, NRR

R. Barrett, NRR

G. Holahan, NRR

B. Bateman, NRR

S. Bajwa, NRR

S. Long, NRR

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U.S. NUCLEAR REGULATORY COMMISSION

REGION III

Docket No:

50-346

License No:

NPF-3

Report No:

50-346/02-08

Licensee:

FirstEnergy Nuclear Operating Company

Facility:

Davis-Besse Nuclear Power Station

Location:

5501 North State Route 2

Oak Harbor, OH 43449

Dates:

May 15 through August 9, 2002

Inspectors:

J. Gavula, Senior Reactor Inspector

M. Farber, Senior Reactor Inspector

J. Jacobson, Senior Mechanical Engineer

Approved by:

John A. Grobe, Chairman

Davis-Besse Oversight Panel

ii

SUMMARY OF FINDINGS

IR 05000346-02-08, on 05/15-08/09/2002, FirstEnergy Nuclear Operating Company,

Davis-Besse Nuclear Power Station. Augmented Inspection Team Follow-up Special

Inspection.

The report covers a special inspection, by three regional inspectors, that focused on

compliance with USNRC rules and regulations as they relate to the facts and circumstances

associated with the degradation of the reactor pressure vessel head. The USNRCs program

for overseeing the safe operation of commercial nuclear power reactors is described in

NUREG-1649, Reactor Oversight Process, Revision 3, dated July 2000.

A.

Inspector Identified Findings

Cornerstones: Initiating Events, Barrier Integrity

Significance to be Determined (TBD). The inspectors identified an apparent

violation of Technical Specification Limiting Condition for Operation for Reactor

Coolant System Operational Leakage, paragraph 3.4.6.2, for operation of the

plant with pressure boundary leakage from through-wall cracks in the reactor

coolant system.

This finding is more than minor because the pressure boundary leakage and

resultant cavity in the reactor vessel head represented a loss of the design basis

barrier integrity. The significance of this finding will be determined by the

Significance Determination Process for the issue, which was begun following the

Augmented Inspection Team activities (Section 4OA3.b.1).

Significance to be Determined (TBD). The inspectors identified an apparent

violation involving failure to take adequate corrective action for a continuing

buildup of boric acid deposits on the reactor head.

This finding is more than minor because the corrosion of the reactor head and

the resulting cavity represented a significant loss of the design basis barrier

integrity. The significance of this finding will be determined by the Significance

Determination Process for the issue, which was begun following the Augmented

Inspection Team activities (Section 4OA3.b.2.1).

Significance to be Determined (TBD). The inspectors identified an apparent

violation involving failure to take adequate corrective action for recurrent

accumulations of boric acid on containment air cooler (CAC) fins. These

accumulations resulted in reduced heat removal capability and reduced air flow

through the cooler which was indicated by decreasing plenum pressure.

This finding is more than minor because the corrosion of the reactor head and

the resulting cavity represented a significant loss of the design basis barrier

integrity. The significance of this finding will be determined by the Significance

iii

Determination Process for the issue, which was begun following the Augmented

Inspection Team activities (Section 4OA3.b.2.2).

Significance to be Determined (TBD). The inspectors identified an apparent

violation involving failure to take adequate corrective action for repeated clogging

of radiation element filters although a sample of the filter deposits revealed iron

oxides, radionuclides, and primary chemistry.

This finding is more than minor because the corrosion of the reactor head and

the resulting cavity represented a significant loss of the design basis barrier

integrity. The significance of this finding will be determined by the Significance

Determination Process for the issue, which was begun following the Augmented

Inspection Team activities (Section 4OA3.b.2.3).

Significance to be Determined (TBD). The inspectors identified an apparent

violation involving the failure to follow the corrective action procedure and take

timely corrective action for a condition adverse to quality, in that the licensee

failed to implement a modification to permit complete inspection and cleaning of

the reactor vessel head and CRDM nozzles.

This finding is more than minor because the corrosion of the reactor head and

the resulting cavity represented a significant loss of the design basis barrier

integrity. The significance of this finding will be determined by the Significance

Determination Process for the issue, which was begun following the Augmented

Inspection Team activities (Section 4OA3.b.2.4).

Significance to be Determined (TBD). The inspectors identified a finding

involving failure to complete an identified corrective action for an adverse trend in

RCS unidentified leakage.

This finding is more than minor because the corrosion of the reactor head and

the resulting cavity represented a significant loss of the design basis barrier

integrity. The significance of this finding will be determined by the Significance

Determination Process for the issue, which was begun following the Augmented

Inspection Team activities (Section 4OA3.b.2.5).

Significance to be Determined (TBD). The inspectors identified an apparent

violation involving deficiencies in the licensees Boric Acid Corrosion Control

procedure, NG-EN-00324.

This finding is more than minor because the corrosion of the reactor head and

the resulting cavity represented a significant loss of the design basis barrier

integrity. The significance of this finding will be determined by the Significance

Determination Process for the issue, which was begun following the Augmented

Inspection Team activities (Section 4OA3.b.3.1).

Significance to be Determined (TBD). The inspectors identified an apparent

violation involving multiple examples of failure to follow the boric acid corrosion

control procedure.

iv

This finding is more than minor because the corrosion of the reactor head and

the resulting cavity represented a significant loss of the design basis barrier

integrity. The significance of this finding will be determined by the Significance

Determination Process for the issue, which was begun following the Augmented

Inspection Team activities (Section 4OA3.b.3.2).

Significance to be Determined (TBD). The inspectors identified an apparent

violation involving two examples of failure to follow the stations corrective action

program procedure.

This finding is more than minor because the corrosion of the reactor head and

the resulting cavity represented a significant loss of the design basis barrier

integrity. The significance of this finding will be determined by the Significance

Determination Process for the issue, which was begun following the Augmented

Inspection Team activities (Section 4OA3.b.3.3).

Significance to be Determined (TBD). The inspectors identified an apparent

violation of 10 CFR 50.9 involving multiple examples of information provided to

the Commission or required by the Commissions regulations to be maintained

by the licensee that were not complete and accurate.

Completeness and accuracy in the documents associated with this issue would

have provided an earlier alert to licensee staff and the USNRC about the

problems with control rod drive mechanism nozzle leakage or may have caused

the USNRC to establish a different regulatory position concerning the urgency of

inspections for the reactor pressure vessel head. The significance of this

apparent violation requires additional review as specified in NUREG-1600,

General Statement of Policy and Procedures for USNRC Enforcement (Section

4OA3.b.4).

B.

Licensee Identified Findings

None

1

Report Details

4.

OTHER ACTIVITIES (OA)

4OA3 Event Follow-up (93812)

Background

On March 6, 2002, Davis-Besse personnel notified the USNRC that reactor vessel head

material, adjacent to a control rod drive nozzle, was significantly degraded. An

Augmented Inspection Team (AIT) was chartered and dispatched to the site on

March 12, 2002, to determine the facts and circumstances related to the reactor vessel

head pressure boundary material degradation, and to identify any precursor indications

of this condition. In accordance with USNRC procedures, the AIT charter did not

include the verification of compliance with USNRC rules and regulations, nor the

recommendation of enforcement actions. The AIT concluded its inspection on April 5,

2002, and issued USNRC Inspection Report 50-346/02-03 on May 3, 2002.

a.

Inspection Scope

The purpose of this current inspection effort was to characterize any regulatory issues

revealed during the AITs activities. The inspection scope included a review of the AIT

report, and also encompassed further reviews of licensee activities related to technical

specification and procedural adequacy and compliance, and corrective action adequacy.

This inspection was based on the facts and circumstances discussed in the AIT report

and will not replicate chronologies or technical analyses unless needed to establish

regulatory basis.

In addition to the information in the AIT report, subsequent questions were raised

regarding completeness and accuracy of documents either required by the USNRC to

be maintained by the licensee or submitted to the USNRC. Consequently, as licensee

documents associated with this issue were reviewed for regulatory compliance,

they were concurrently reviewed for completeness and accuracy. Because the risk

significance of the reactor vessel head degradation has not been finalized, and several

of these apparent violations remain under review by the USNRC, all of the findings will

be classified as Unresolved Items in accordance with Manual Chapter 0612, Power

Reactor Inspection Reports.

b.

Findings

b1.

Technical Specification Reactor Coolant System (RCS) Operational Leakage

a.

Introduction

The inspection identified an apparent violation, whose significance is yet to be

determined, involving the Davis-Besse technical specification associated with operation

of the plant with pressure boundary leakage from through-wall cracks in the RCS. This

2

finding had a credible impact on safety and was characterized as an unresolved item

(URI) pending USNRC determination of the significance of the apparent violation.

b.

Description

On February 27 and March 5, 2002, the licensee notified the USNRC that their

evaluation of ultrasonic test data, for axial indications in control rod drive mechanism

nozzles Nos. 1, 2, and 3, confirmed that there was reactor pressure boundary leakage.

Further investigation revealed a cavity adjacent to control rod drive penetration nozzle

No. 3, approximately 5 to 7 inches long and 4 to 5 inches wide. Within this area, the

6.63 inch- thick low-alloy steel head had been corroded away, leaving only the stainless

steel cladding layer on the inside of the reactor vessel head. Based on the length of the

cracks, the amount of boric acid accumulation on the reactor vessel head, and the

extensive corrosion of the reactor vessel head, it is clear that the unit operated well in

excess of 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br /> with pressure boundary leakage.

At the time of plant shutdown, the unidentified primary coolant system leak rate was

approximately 0.2 gpm, within the Technical Specification 3.4.6.2.b limit of 1.0 gpm.

However, Technical Specification 3.4.6.2.a requires that primary coolant operational

leakage shall be limited to No PRESSURE BOUNDARY LEAKAGE when in Modes 1-

4. The associated action requires that the plant be placed in Hot Standby within 6 hours6.944444e-5 days <br />0.00167 hours <br />9.920635e-6 weeks <br />2.283e-6 months <br />

and in Cold Shutdown within the following 30 hours3.472222e-4 days <br />0.00833 hours <br />4.960317e-5 weeks <br />1.1415e-5 months <br />. Although the time the pressure

boundary leakage began could not be precisely determined, it is clear that the leakage

existed greater than the time frame that would have required plant shutdown.

c.

Analysis

This issue represented a licensee performance deficiency because the licensee had

multiple opportunities over a period of years to identify the leakage; consequently it was

considered a finding. This finding is of more than minor safety significance because the

pressure boundary leakage and resultant cavity in the reactor vessel head represented

a loss of the design basis barrier integrity. Two cornerstones were impacted by this

issue. The Barrier Integrity cornerstone was affected because the through-wall CRDM

cracks compromised the reactor coolant pressure boundary and the Initiating Events

cornerstone was impacted because cracking of the CRDM nozzles resulted in an

increase in the likelihood of a loss of coolant accident (LOCA). The significance of this

finding will be determined by the Significance Determination Process (SDP) for the

issue, which was begun following the AIT activities.

d.

Enforcement

Davis-Besse Technical Specification, Limiting Condition for Operation for Reactor

Coolant System Operational Leakage, paragraph 3.4.6.2, states, in part, that RCS

leakage shall be limited to no pressure boundary leakage, and that with any pressure

boundary leakage, the unit is to be in Cold Shutdown within 36 hours4.166667e-4 days <br />0.01 hours <br />5.952381e-5 weeks <br />1.3698e-5 months <br />. This issue is

encompassed within the licensee root cause analysis, conducted for Condition Report

(CR) 2002-01128. There is no current safety concern because the plant is presently

shut down, cooled down, and defueled. Because the safety significance of the apparent

violation has yet to be determined, the noncompliance will be classified as an

3

unresolved item. This will be identified as URI 50-346/02-08-01, Reactor Operation

with Pressure Boundary Leakage.

b.2

Corrective Action

b.2.1 Reactor Head Boric Acid Deposits

a.

Introduction

The inspectors identified an apparent violation, whose significance is yet to be

determined, involving failure to take adequate corrective action for a continuing buildup

of boric acid deposits on the reactor head. This finding had a credible impact on safety

and was characterized as a URI pending USNRC determination of the significance of

the apparent violation.

b.

Description

A series of Potential Condition Adverse to Quality Reports (PCAQR) and Condition

Reports (CR) from 1990 through 2001 tracks recurrent identification of boric acid

deposits on the reactor head. Section XI of the American Society of Mechanical

Engineers (ASME) Boiler and Pressure Vessel Code IWA-5250, requires that the

leakage source and areas of general corrosion be located when boric acid residues are

detected on components. Section 4.3 of the AIT report (IR 50-346/02-03(DRS))

provides a chronology of reactor head inspections which identify boric acid deposits on

the reactor head and how the licensees engineering staff evaluated and dispositioned

each occurrence.

Through much of the early operating years until the mid-1990s, CRDM flanges at

Davis-Besse were prone to developing leaks during the operating cycle. This leakage

was evidenced by boric acid deposits on the flange, the service structure, and on the

reactor head (due to leakage which ran down the nozzles between the nozzles and the

insulation). Beginning with the plants sixth refueling outage (RFO) in 1990, the licensee

began systematically correcting these leaks by replacing the flange gasket with a new

design. As this program was implemented the frequency of CRDM flange leakage was

reduced. By end of the tenth RFO in 1996, all the flanges had the redesigned gasket

installed.

Beginning with the tenth RFO in 1996 and proceeding through the twelfth RFO in 2000,

six PCAQRs and CRs documented the identification of boric acid deposits on the

reactor head and the licensee engineering staffs disposition of the conditions. Each of

these presented an opportunity to identify nozzle leakage. Collectively, they revealed a

focus on CRDM flange leakage as the source of boric acid deposits despite evidence

that the deposits must be from another source. For example, rust-colored deposits,

indicative of iron, could not likely have come from the flanges which were stainless steel.

Corrosion of the split ring nuts associated with the flanges would not have resulted in

the quantity of corrosion products entrained in the deposits on the head. Finally, there

were significant accumulations of boric acid on the head during operating cycles where

CRDM flange leakage was non-existent or considered negligible.

4

c.

Analysis

This issue represented a performance deficiency because the licensee failed to properly

address, either individually or collectively, the continuing accumulation of large amounts

of boric acid on the reactor head, a significant condition adverse to quality. This lack of

adequate corrective action on the licensees part, contributed to the failure to detect

existing through-wall CRDM nozzle cracks.

This finding is more than minor because the corrosion of the reactor head and the

resulting cavity represented a significant loss of the design basis barrier integrity. Two

cornerstones were impacted by this issue. The Barrier Integrity cornerstone was

affected because the through-wall CRDM cracks compromised the reactor coolant

pressure boundary and the Initiating Events cornerstone was impacted because

cracking of the CRDM nozzles resulted in an increase in the likelihood of a LOCA. The

significance of this finding will be determined by the Significance Determination Process

(SDP) for the issue, which was begun following the AIT activities.

d.

Enforcement

10 CFR Part 50, Appendix B, Criterion XVI, states in part, that measures shall be taken

to ensure that conditions adverse to quality such as failures, malfunctions, deficiencies,

deviations, defective material and equipment, and nonconformances are promptly

identified and corrected. Criterion XVI also requires that for significant conditions

adverse to quality, the measures shall assure that the cause of the condition is

determined and that corrective actions are taken to preclude repetition. The failure to

properly address the recurrent accumulation of boric acid deposits on the reactor head,

a significant condition adverse to quality, contributed to the corrosion of the reactor

head. There is no current safety concern because the plant is presently shut down,

cooled down, and defueled. Because the safety significance of the apparent violation

has yet to be determined, the noncompliance will be classified as an unresolved item.

This will be identified as URI 50-346/02-08-02, Reactor Vessel Head Boric Acid

Deposits.

b.2.2 Containment Air Cooler Deposits

a.

Introduction

The inspectors identified an apparent violation whose significance is yet to be

determined involving failure to take adequate corrective action for recurrent

accumulations of boric acid on containment air cooler (CAC) fins. These accumulations

resulted in reduced air flow through the cooler which was indicated by decreasing

plenum pressure. This finding had a credible impact on safety and was characterized

as an unresolved item pending USNRC determination of the significance of the apparent

violation.

b.

Description

The inspectors reviewed one PCAQR and three CRs spanning the period

November 1998 through January 2001. Section 5.3 of the AIT report

5

(IR 50-346/02-03(DRS)) provides a chronology of CAC fouling and how the

licensees engineering staff evaluated and dispositioned each occurrence.

At the onset of the leak, CRDM nozzle leakage created an aerosol of steam, boric acid,

and other contaminants in the air space above the head. The steam and aerosol

particles were picked up by the service structure ventilation system intake and

distributed throughout the containment. The CACs subsequently condensed the steam

and the boric acid plated out on the cooler fins. Later, as the corrosion of the head

progressed, the aerosol consisted of steam, boric acid, and corrosion particles.

Consistent with this, the deposits on the cooler fins changed color from white to red-

brown.

The licensees attempts to address this phenomenon focused on maintaining operability

of the coolers through frequent cleanings of the coolers. Of the four corrective action

documents examined, only one considered the source of the boric acid deposits;

however, no actions to investigate the source were prescribed. Of particular

significance was the licensees evaluation of the July 1999 appearance of rust-colored

deposits. The licensee continued to attribute the boric acid deposits to CRDM flange

leakage; the discoloration of the boric acid was attributed to migration of the surface

corrosion on the CACs into the boric acid and the aging of the boric acid itself.

c.

Analysis

This issue represented a performance deficiency because the licensee failed to properly

address, either individually or collectively, the cause for the recurrent deposition of boric

acid on CAC fins, nor the change in the color of the deposits, although the change was

indicative of carbon steel corrosion. This lack of adequate corrective action on the

licensees part contributed to their failure to detect existing through-wall CRDM nozzle

cracks and the reactor pressure vessel head corrosion.

This finding is more than minor because the corrosion of the reactor head and the

resulting cavity represented a significant loss of the design basis barrier integrity. Two

cornerstones were impacted by this issue. The Barrier Integrity cornerstone was

affected because the through-wall CRDM cracks compromised the reactor coolant

pressure boundary and the Initiating Events cornerstone was impacted because

cracking of the CRDM nozzles resulted in an increase in the likelihood of a LOCA. The

significance of this finding will be determined by the Significance Determination Process

(SDP) for the issue, which was begun following the AIT activities.

d.

Enforcement

10 CFR Part 50, Appendix B, Criterion XVI, states in part, that measures shall be taken

to ensure that conditions adverse to quality such as failures, malfunctions, deficiencies,

deviations, defective material and equipment, and nonconformances are promptly

identified and corrected. Criterion XVI also requires that for significant conditions

adverse to quality, the measures shall assure that the cause of the condition is

determined and that corrective actions are taken to preclude repetition. The failure to

properly address the recurrent deposits of boric acid deposits on the CAC fins, a

significant condition adverse to quality, contributed to the corrosion of the reactor head.

6

There is no current safety concern because the plant is presently shut down, cooled

down, and defueled. Because the safety significance of the apparent violation has yet

to be determined, the noncompliance will be classified as an unresolved item. This will

be identified as URI 50-346/02-08-03, Containment Air Cooler Boric Acid Deposits.

b.2.3 Radiation Element Filter Deposits

a.

Introduction

The inspectors identified an apparent violation, whose significance is yet to be

determined, involving failure to take adequate corrective action for repeated clogging of

radiation element filters, although a sample of the filter deposits revealed iron oxides,

and radionuclides indicative of reactor coolant. This finding had a credible impact on

safety and was characterized as a URI pending USNRC determination of the

significance of the apparent violation.

b.

Description

Starting in May 1999, yellowish-brown material began to accumulate on the radiation

element filters, causing repetitive, degraded performance of the containment radiation

monitors due to low flow. Condition Report 99-0882 issued on May 13, 1999, identified

low flow conditions on radiation element 4597BA. The CR noted that the apparent

cause was boric acid particles collecting on the filter at a very high rate. The licensee

subsequently sent a sample of the material for analysis, and in August 1999, Southwest

Research Institutes Report No. 18-2321-190 concluded that the deposits on the filters

were a powdery iron oxide and were likely corrosion products from an iron-based

component within the system. The licensee initiated Condition Report 1999-1300 on

May 23, 1999, to document this issue, and noted that Plant Engineering was to issue an

Action Plan for the 12 RFO which would include containment walkdowns to identify

possible sources of the rust particles. Sargent and Lundy was subsequently asked to

review the report, and on November 5, 1999, their response letter stated:

The fineness of the iron oxide (assumed to be ferric oxide) particulate

would indicate it probably was formed from a very small steam leak. The

particulate was likely originally ferrous hydroxide in small condensed

droplets of steam and was oxidized to ferric oxide in the air before it

settled on the filters; and the iron oxide does not appear to be coming

from the general corrosion of a bare metal surface in containment or from

steam impingement on a metal surface.

Although the licensee conducted containment entries at power to identify the source

of the apparent steam leak, it was never identified. After the 12th RFO in May 2000,

the radiation element filters continued to clog with corrosion products. CR 01-1110

was issued on April 23, 2001, to document continued clogging of the radiation monitor

filters due to boric acid build-up. Corrective action was to move the sample point.

CR 01-1822 dated July 23, 2001, documented increased frequency of monitor filter

change outs again, due to boric acid clogging. Disposition of this CR was to continue to

change the filters until an upcoming refueling outage could identify the source of RCS

leakage. CR 01-2795, dated October 22, 2001, again identified a high frequency of filter

7

clogging, noting that previous corrective actions were unsuccessful. Corrective action

for this CR was to perform a temporary modification (TM 01-0019) to remove the filter

cartridge.

c.

Analysis

This issue represented a performance deficiency because the licensee failed to take

appropriate corrective action (identify and repair the source of the RCS leakage) for a

significant condition adverse to quality, in that, the filters clogged with a material

indicative of RCS leakage and corrosion products and this continued for more than two

years. It has subsequently been concluded that the material clogging the filters was

from the ongoing corrosion of the reactor vessel head. While some containment

walkdowns were conducted, the source of the RCS leakage was not identified.

Furthermore, the corrective actions implemented for the CRs written on this problem

appeared to focus on the operability of the radiation monitors and not the root cause

(i.e., RCS leakage and corrosion). This lack of adequate corrective action on the

licensees part, contributed to their failure to detect existing through-wall CRDM nozzle

cracks.

This finding is more than minor because it affected the Initiating Events cornerstone

objective in that cracking of CRDM nozzles represented an increase in the likelihood of

a LOCA. The Barrier Integrity cornerstone was also affected in that CRDM cracks

resulted in leakage through the reactor coolant pressure boundary. The significance of

this finding will be determined by the Significance Determination Process (SDP) for the

issue, which was begun following the AIT activities.

d.

Enforcement

10 CFR Part 50, Appendix B, Criterion XVI, requires, in part, that conditions adverse to

quality be promptly identified and corrected. Criterion XVI also requires that for

significant conditions adverse to quality, the measures shall assure that the cause of the

condition is determined and that corrective actions are taken to preclude repetition.

Contrary to this, the licensee failed to correct the condition identified in CR 99-0882,

initiated on May 13, 1999. As of February 16, 2002, the source of the RCS leakage had

not been identified and corrected. There is no current safety concern because the plant

is presently shut down, cooled down, and defueled. Because the safety significance of

this apparent violation has yet to be determined, it will be classified as an unresolved

item. This will be identified as URI 50-346/02-08-04, Radiation Element Filters.

b.2.4 Service Structure Modification

a.

Introduction

An apparent violation whose significance is yet to be determined, was identified for the

failure to implement the corrective action procedure and take prompt corrective action

for a condition adverse to quality. The licensee failed to implement a modification to

permit complete inspection and cleaning of the reactor vessel head and CRDM nozzles.

This finding had a credible impact on safety and was characterized as a URI pending

USNRC determination of risk significance.

8

b.

Description

USNRC Generic Letter 88-05 was issued on March 17, 1988, and notified licensees of

the potential for boric acid degradation of carbon steel reactor pressure boundary

components. On May 28, 1993, BAW issued document BAW 10190P, Safety

Evaluation for BAW Design Reactor Vessel Head Control Rod Drive Mechanism Nozzle

Cracking. This document stated that B&WOG utilities developed plans to visually

inspect the CRDM nozzle area to determine if through wall cracking had occurred. If

any leaks or boric acid crystal deposits were located, an evaluation of the source of the

leak and the extent of any wastage was to be evaluated. The USNRC notified

NUMARC of the results of the USNRC safety evaluation related to this subject on

November 19, 1993. This safety evaluation concluded that there was no current safety

concern for cracking of CRDM penetrations. The conclusion was predicated on the

performance of the visual inspection activities requested in Generic Letter 88-05.

Modification 90-0012 was initiated during RFO 6 on March 21, 1990, to install multiple

access ports in the service structure to permit cleaning and inspection of the reactor

head. At this time, it was noted that boric acid had leaked down from the CRD flanges

and accumulated on the head, thus subjecting the head to potential degradation. This

modification was not performed during the next two refuel outages (RFO 7 and 8) and

was subsequently voided on September 27, 1993, noting that the head had been

successfully inspected with cameras and cleaned during the previous three refuel

outages (utilizing existing small mouse holes holes in the service structure).

Modification 94-0025 was initiated on May 27, 1994, again to install access ports in the

service structure to permit cleaning and inspection of the head. Reasons cited for the

modification were that video inspections (through existing mouse holes) were difficult

and not always adequate and that inspection and cleaning of 100 percent of the head

could not be accomplished without performing the modification. This modification was

not performed during RFO 9 (October 1, 1994) and a decision was made on June 15,

1995, to defer scheduling it for RFO 10 (April 8, 1996) pending further industry

information/investigation concerning actual benefit. During a meeting of the Work

Scope Committee (WSC) on February 20, 1997, a decision was made to reschedule the

modification for RFO 12 (April 1, 2000). Subsequently, during a meeting of the WSC on

September 17, 1998, the modification was again rescheduled, this time, for RFO 13

(February 16, 2002).

Potential Condition Adverse to Quality 96-0551 was initiated on April 21, 1996, to

address the inability to comply with some of the provisions of NG-EN-00324 (Boric Acid

Corrosion Control Program) with respect to inspection and cleaning of the head during

RFO 10. This PCAQR stated, in part, Since the boric acid deposits are not cleaned it is

difficult to distinguish whether the deposits occurred because of the leaking flanges or

the leaking CRDM. This situation represents an adverse trend with the potential for

greater than marginal consequences. The PCAQR further states, The extent of the

inspection was limited to approximately 50 to 60 percent of the head area because of

the restrictions imposed by the location and size of mouse holes. Modification 94-0025

was specified as the corrective action for this PCAQR.

9

c.

Analysis

This issue represented a performance deficiency because the licensee failed to take

corrective action (install the access port modification) for a condition adverse to quality.

As noted above, from the information in Modification 94-0025 and PCAQR 96-0551, it is

apparent that complete inspection and cleaning of the head could not be performed

without installing the access ports. As of February 16, 2002, the modification had not

been performed, the head had not been completely inspected, and the head had not

been completely cleaned. This lack of action on the licensees part, contributed to their

failure to detect existing through-wall CRDM nozzle cracks.

This finding is more than minor because it affected the Initiating Events cornerstone

objective in that cracking of CRDM nozzles represented an increase in the likelihood of

a LOCA. The Barrier Integrity cornerstone was also affected in that CRDM cracks

resulted in leakage through the reactor coolant pressure boundary. Furthermore, the

failure to provide for adequate inspection and cleaning of the head was a contributing

factor to the head degradation. The significance of this finding will be determined by the

SDP for the issue, which was begun following the AIT activities.

d.

Enforcement

10 CFR Part 50, Appendix B, Criterion V, requires, in part, that activities affecting quality

be accomplished in accordance with written procedures. The licensee failed to follow its

corrective action procedure and correct the condition identified on April 21, 1996

(inability to fully inspect the head and CRDM nozzles), in that, as of February 16, 2002,

the corrective action (modification of the service structure) had not been accomplished.

There is no current safety concern because the plant is presently shut down, cooled

down, and defueled. The service structure has since been modified to permit complete

inspection and cleaning of the head. Because the safety significance of this apparent

violation has yet to be determined, it will be classified as an unresolved item. This will

be identified as URI 50-346/02-08-05, Service Structure Modification Delay.

b.2.5 Reactor Coolant System Unidentified Leakage Trend

a.

Introduction

The inspectors identified a finding whose significance is yet to be determined involving

failure to follow the corrective action procedure and complete a prescribed corrective

action for adverse trends in RCS unidentified leakage. This finding had a credible

impact on safety and was characterized as an unresolved item pending USNRC

determination of the significance of the apparent violation.

b.

Description

In 1998, shortly after completing the eleventh RFO, the licensee identified a sharp rise in

RCS unidentified leakage which had been relatively stable at 0.05 gpm. This was

attributed to a temporary modification which bypassed a pressurizer relief valve drain

line and allowed leakage past the relief valves to be vented directly into the containment

atmosphere. This leakage collected in the normal sump and added to the unidentified

10

leakage, which increased to a maximum of 0.8 gpm. During a mid-cycle outage in May

of 1999, the licensee resolved this issue by installing new rupture disks and

reconnecting the drain line. This resulted in a decrease in unidentified leakage.

However, the unidentified leakage returned to levels between 0.15 and 0.25 gpm.

The inspectors reviewed a series of four CRs which demonstrated that the licensee was

aware of the increase in unidentified leakage, and becoming increasingly concerned by

their inability to identify the source. The engineering evaluation into the issue became

more involved with each succeeding CR. CR 2001-2862 contained a detailed evaluation

and a corrective action to develop a containment inspection plan for the forthcoming

RFO. This inspection plan was completed and documented in the CR. It involved

coordination of four actions: the Mode 3 (reactor shutdown, normal operating

temperature and pressure) walkdown, mode 5 (cold shutdown) RCS walkdowns, Boric

acid corrosion control walkdowns, and the ASME VT-2 examinations. The inspectors

determined that proposed corrective actions associated with RCS unidentified leakage

were adequate; however, a key action, the mode 3 walkdown was subsequently

canceled. This significantly reduced the quality of the proposed corrective action to the

point where it was no longer adequate.

c.

Analysis

This issue represented a licensee performance deficiency because elimination of a key

component of what was an adequate proposed corrective action rendered the proposal

inadequate. Consequently, this was considered a finding. This finding was of more

than minor safety significance because the corrosion of the reactor head and the

resulting cavity represented a significant loss of the design basis barrier integrity. Two

cornerstones were impacted by this issue. The Barrier Integrity cornerstone was

affected because the through-wall CRDM cracks compromised the reactor coolant

pressure boundary and the Initiating Events cornerstone was impacted because

cracking of the CRDM nozzles resulted in an increase in the likelihood of a LOCA. The

significance of this finding will be determined by the SDP for the issue, which was begun

following the AIT activities.

d.

Enforcement

The licensee failed to follow the corrective action procedure and implement an effective

corrective action for adverse trends in RCS unidentified leakage. There is no current

safety concern because the plant is presently shut down, cooled down, and defueled.

Because the safety significance of this finding has yet to be determined, it will be

classified as an unresolved item. This will be identified as URI 50-346/02-08-06,

Reactor Coolant System Unidentified Leakage Trend.

11

b.3

Procedures

b.3.1 Procedures Not Appropriate to the Circumstances

a.

Introduction

The inspectors identified an apparent violation whose significance is yet to be

determined, involving deficiencies in the licensees Boric Acid Corrosion Control

procedure, NG-EN-00324. This finding had a credible impact on safety and was

characterized as an unresolved item pending USNRC determination of the significance

of the apparent violation.

b.

Description

The inspectors reviewed the original and subsequent revisions, up to the date of

discovery of the reactor head conditions, of the licensees Boric Acid Corrosion Control

Program, NG-EN-00324. The purpose of the review was to assess the adequacy of the

procedure and determine whether any deficiencies may have contributed to the event.

The inspectors noted the following weaknesses in the procedure:

a.

The procedure had a clear focus on bolted, flanged connections. Seven

of nine principal locations in Section 6.1.1, the definition of an RCS

pressure boundary component in Section 4.9, and the definitions of minor

(Section 4.2), moderate (Section 4.3), and substantial (Section 4.4)

leakage all contained references to bolted connections.

b.

In Section 6.3.4, the procedure directed preparation of a CR, repair tag,

or work order if a detailed inspection was warranted, but guidance,

specifications, or thresholds for initiating a detailed inspection were

inadequate.

c.

The inspectors determined that preparation of a repair tag or work order

in lieu of a CR was inappropriate because it only addressed the symptom

by fixing the leak rather than evaluate why the leak was occurring.

d.

Qualifications for Plant Engineering staff conducting inspections and

evaluations were not addressed. This resulted in inconsistencies in

inspection techniques, observations, recording of results, and

evaluations.

e.

In section 6.3.1.f, the procedure exempted stainless steel or inconel

components from further examination related to boric acid corrosion,

unless the examination was during an ASME Section XI test which might

require a bolting examination. However, there was industry experience

dating back to 1990, including an USNRC Information Notice, identifying

primary water stress corrosion cracking of stainless steel, due to boric

acid attack, as a concern.

12

f.

The procedure did not require maintenance of any documents, such

as checklists or evaluations, although the procedure is quality related

and Davis-Besse Supplemental Procedure Requirements/Guidance,

NG-QS-00120 stated in Attachment 2, Section1.2.b that these

procedures were used to assure safe operation.

The inspectors determined that these weaknesses collectively contributed to the

corrosion of the reactor head, either through narrowing the scope of inspection

or failing to provide adequate instruction for carrying out activities.

c.

Analysis

This issue represented a licensee performance deficiency because the weaknesses in

the procedure contributed to the failure, over a period of years, by the licensees

engineering staff to properly identify and evaluate the leaking CRDM nozzle and the

expanding cavity in the reactor head. Consequently, this was considered a finding. This

finding was of more than minor safety significance because the cavity in the reactor

vessel head represented a loss of the design basis barrier integrity. The significance of

this finding will be determined by the SDP for the issue, which was begun following the

AIT activities.

d.

Enforcement

10 CFR Part 50, Appendix B, Criterion V, states, in part, that activities affecting quality

shall be prescribed by documented instructions, procedures, or drawings, of a type

appropriate to the circumstances and shall be accomplished in accordance with these

instructions, procedures, or drawings. NG-EN-00324, Boric Acid Corrosion Control

Program, Revisions 0 through 2, were classified as a quality procedure under the

licensees procedure administrative system and were not appropriate to the

circumstances in that deficiencies in the procedure contributed to the failure to detect

and address corrosion of the reactor head. There is no current safety concern because

the plant is presently shut down, cooled down, and defueled. Because the safety

significance of the apparent violation has yet to be determined, the noncompliance will

be classified as an unresolved item. This will be identified as URI 50-346/02-08-07,

Inadequate Boric Acid Corrosion Control Program Procedure.

b.3.2 Failure to Follow Boric Acid Corrosion Control Program Procedure

a.

Introduction

The inspectors identified an apparent violation whose significance is yet to be

determined involving multiple examples of failure to follow the boric acid corrosion

control procedure. This finding had a credible impact on safety and was characterized

as an unresolved item pending USNRC determination of the significance of the apparent

violation.

13

b.

Description

The inspectors reviewed a series of PCAQRs and CRs that documented occurrences of

the licensees failure to adhere to the instructions in the Boric Acid Corrosion Control

Program procedure.

PCAQR 96-0551 (in RF010) recorded that a visual inspection of the head

showed boric acid accumulation on the head and that CRDM nozzle No. 67 had

rust-colored deposits where it penetrated the head. The PCAQR further records

that inspection of CRDM nozzle No. 67 flange showed no signs of leakage

during the operating cycle, signifying that the present deposits were the result of

leakage from previous operating cycles. The conclusion drawn from these two

statements was that, as a minimum, boric acid deposits were not removed from

the head, nor was the base metal inspected for corrosion during RF09 as

directed by the boric acid corrosion control program procedure.

PCAQRs 98-0649 and 98-0767 (in RF011) both recorded visual inspections of

the reactor head using a video camera on April 17, 1998, and April 24, 1998,

respectively. Both inspections revealed boric acid residue on the head.

PCAQR 98-0649 focused on CRDM flange D-10 which was determined to have

minor leakage, based on the amount of boric acid on the flange. A review of

unidentified leakage was conducted and average unidentified leakage during the

previous operating cycle was 0.05 gallons per minute. Based on this

information, repair of flange D-10 was deferred. PCAQR 98-0767 recorded that

most of the head area was covered with an uneven layer or boric acid along

with some lumps of boric acid. The color of the layer and the lumps varied from

rust brown to white. The rust or brown color is an indication of the old boric acid

deposits. The conclusion drawn from these two PCAQRs is that boric acid

deposits were left on the head at the end of the tenth RFO and that the base

metal under these deposits was not inspected as directed by the boric acid

corrosion control program procedure.

PCAQR 98-0767 (RF011) records that the reactor head was cleaned as best we

can. Later the PCAQR records that an inspection after the cleaning showed

there were boric acid deposits left on the head after the cleaning. At the end of

RF011, the base metal under these deposits was not inspected as directed by

the boric acid corrosion control program procedure.

CRs 2000-0781, 2000-0782, and 2000-1037 (RF012) were all written to

document the extensive build-up of boric acid residue on the reactor head.

CR 2000-0782 describes the conditions in detail and photographs of the head

near the closure studs were included. Among the corrective actions specified in

the condition report was cleaning boric acid deposits off the head in accordance

with work order 00-001846-000. A video tape made after this cleaning showed

that a thick layer of red/brown boric acid deposits remained around the nozzles

near the center of the head. At the end of the twelfth RFO, the base metal under

these deposits was not inspected as directed by the boric acid corrosion control

program procedure.

14

c.

Analysis

This issue represented a licensee performance deficiency because the recurrent

failures, by the licensees engineering staff, to remove boric acid deposits and inspect

the base metal of the reactor head as directed by the boric acid corrosion control

procedure, resulted in the perpetuation of the CRDM nozzle leak and the development

of the expanding cavity in the reactor head. Consequently, this was considered a

finding. This finding was of more than minor safety significance because the cavity in

the reactor vessel head represented a loss of the design basis barrier integrity. The

significance of this finding will be determined by the SDP for the issue, which was begun

following the AIT activities.

d.

Enforcement

10 CFR Part 50, Appendix B, Criterion V, states, in part, that activities affecting quality

shall be prescribed by documented instructions, procedures, or drawings, of a type

appropriate to the circumstances and shall be accomplished in accordance with these

instructions, procedures, or drawings. The licensees engineering staff failed, on

multiple occasions, to remove boric acid deposits and inspect the base metal of the

reactor head as directed by NG-EN-00324, Revision 2, Boric Acid Corrosion Control

Program. This issue is encompassed within the licensee root cause analysis,

prescribed by CR 2002-01128. There is no current safety concern because the plant is

presently shut down, cooled down, and defueled. Because the safety significance of the

apparent violation has yet to be determined, the noncompliance will be classified as an

unresolved item. This will be identified as URI 50-346/02-08-08, Failure to Follow Boric

Acid Corrosion Control Program Procedure.

b.3.3 Failure to Follow Corrective Action Program Procedure

a.

Introduction

The inspectors identified an apparent violation whose significance is yet to be

determined involving two examples of failure to follow the stations corrective action

program procedure. This finding had a credible impact on safety and was characterized

as an unresolved item pending USNRC determination of the significance of the apparent

violation.

b.

Description

CRs 2000-0782, and 2000-1037 (RF012) were written to document the extensive

build-up of boric acid residue on the reactor head. CR 2000-0782 described the

conditions in detail and photographs of the head near the closure studs were included.

CR 2000-1037 described the analysis (deferring in part to CR 2000-0782) and the

cleaning effort. In both CRs the extent and significance of the boric acid deposits, and

that such build-up was recurrent, were clear. The quantity of boric acid deposits

accumulated was highly unusual, extensive corrective actions were necessary, and an

adverse repetitive trend existed.

15

Attachment 2, Categorization of Condition Report, to NG-NA-00702, Revision 3,

Corrective Action Program, provides guidance and examples for characterization of

condition reports as significant, important, routine, or non-conditions adverse to quality.

Among the examples of significant conditions are:

Issues of collective significance that considered individually may not be

significant, but as a whole indicate problems that warrant root cause

investigation and corrective action to prevent recurrence.

Substantial deviations, deficiencies in construction or design, damage such that

extensive corrective actions are required.

A repetitive or adverse trend exists.

During RF012, the engineering staff was aware of the continuing accumulation of boric

acid on the reactor head; the problem had been documented in PCAQRs and CRs since

1996. Although the quantity of boric acid deposits was a substantial deviation from

acceptable operating conditions for the reactor head, the history of reactor head boric

acid deposits revealed a significant problem, and that a repetitive, adverse trend existed.

Both condition reports were classified as routine.

c.

Analysis

This issue represented a licensee performance deficiency. A proper characterization of

condition reports 2000-0782 and 2000-1037 would have resulted in a formal root cause

evaluation as prescribed by the licensees Root Cause Analysis Reference Guide.

Incorrectly characterizing these CRs as routine resulted in an apparent cause

determination with no required corrective actions to prevent recurrence; an opportunity

to identify the true nature of the leak and the growing cavity in the head was missed.

Consequently, this was considered a finding. This finding was of more than minor

safety significance because the cavity in the reactor vessel head represented a loss of

the design basis barrier integrity. The significance of this finding will be determined by

the SDP for the issue, which was begun following the AIT activities.

d.

Enforcement

10 CFR Part 50, Appendix B, Criterion V, states, in part, that activities affecting quality

shall be prescribed by documented instructions, procedures, or drawings, of a type

appropriate to the circumstances and shall be accomplished in accordance with these

instructions, procedures, or drawings. The licensee failed to properly characterize

CRs 2000-0782 and 2000-1037 as significant conditions adverse to quality, in

accordance with the guidance contained in the licensees corrective action program

procedure. This issue is encompassed within the licensee root cause analysis,

prescribed by CR 2002-01128. There is no current safety concern because the plant is

presently shut down, cooled down, and defueled. Because the safety significance of the

apparent violation has yet to be determined, the noncompliance will be classified as an

unresolved item. This will be identified as URI 50-346/02-08-9, Failure to Follow

Corrective Action Program Procedure.

16

b.4

Completeness and Accuracy of Information

a.

Introduction

In addition to the information in the AIT report subsequent questions were raised

regarding completeness and accuracy of documents either required by the USNRC to

be maintained by the licensee or submitted to the USNRC. Consequently, as licensee

documents associated with this issue were reviewed for regulatory compliance, they

were concurrently reviewed for completeness and accuracy in all material respects as

required by 10 CFR 50.9, Completeness and Accuracy of Information.

b.

Description

The inspectors review of the extensive documentation associated with this issue

revealed a series of examples of information provided to the Commission or required by

the Commissions regulations to be maintained by the licensee that were not complete

and accurate.

1.

The cancellation of Modification 90-012 was based on a statement in a

Document Void Request, approved September 23, 1993: Current inspection

techniques using high-powered cameras preclude the need for inspection ports,

additionally, cleaning of the reactor vessel head during last three outages was

completed successfully without requiring access ports. This statement is

inaccurate because boric acid deposits were left on the head at the end of both

the seventh and eighth refueling outages, the two outages preceding this

statement.

2.

PCAQR 98-0649, dated April 18, 1998, made the statement, Accumulation of

boric acid on the reactor vessel caused by leaking CRDMs has not resulted in

any boric acid corrosion. This was identified through inspections following

reactor vessel head cleaning in past outages. This statement is inaccurate

because areas of the reactor head were not cleaned of boric acid deposits nor

was the base metal under all the deposits inspected.

3.

PCAQR 98-0649 also contained the following statement, Additionally, B&W

documentation discussing CRDM nozzle cracking further stated that boric acid

deposits on the head caused by leaking CRDM flanges would not result in head

corrosion. The PCAQR did not state which B&W document was being

referenced. The inspectors reviewed the following documents:

a.

51-1219275-01, CRDM Leakage Detection Evaluation, December 13,

1993

b.

51-1229638-00, Boric Acid Corrosion Data Summary and Evaluation,

April 15, 1994

c.

BAW-10190P, Safety Evaluation for B&W-Design Reactor Vessel Head

Control Rod Drive Mechanism Nozzle Cracking

17

d.

BAW-10190P, Addendum 1, External Circumference Crack Growth

Analysis for B&W-Design Reactor Vessel Head CRDM Nozzles

e.

BAW-10190P, Addendum 2, Safety Evaluation for Control Rod Drive

Mechanism Nozzle J-Groove Weld

f.

B&W Materials Committee Report 51-1201160-00, Alloy 600 SCC

Susceptibility: Scoping Study of Components at Crystal River 3

g.

B&W Report 51-1218440-00, Alloy PWSCC Time-to-Failure Models

h.

B&W Report 51-1219143-00, CRDM Nozzle Characterization

i.

BAW-2301, B&WOG Integrated Response to USNRC Generic Letter 97-

01, Degradation of Control Rod Drive Mechanism Nozzle and Other

Vessel Closure Head Penetrations

The inspectors did not find that statement in any of those nine documents, nor

did the licensee identify the source document for that statement.

4.

PCAQR 98-0767, dated April 25, 1998, Section 4A, Item F, stated, The boric

acid deposits were removed from the head. This is incorrect information; it has

been acknowledged that the head was not completely cleaned at the end of

eleventh RFO.

5.

Condition report CR 2000-1037, dated April 17, 2000, page 6 of 7, under

Remedial Actions stated, Accumulated boron deposited between the reactor

head and the thermal insulation was removed during the cleaning process

performed under W.O. 00-001846. No boric acid induced damage to the head

surface was noted during the subsequent inspection. This statement was

inaccurate in that the accumulated boric acid was only removed from some

areas of the head, and the subsequent inspection of the head surface for boric

acid induced damage was only for that portion of the head where the boric acid

deposit had been removed.

6.

Work Order 00-001846-000, Clean Boron Accumulation from Top of Reactor

Head and Top of Insulation, dated April 25, 2000, was prepared and issued to

clean the reactor head as directed by the boric acid corrosion control procedure.

The Work Order log stated, work performed without deviation. This was

inaccurate since CRs clearly indicated that boric acid deposits were left on the

head after the cleaning.

7.

QA Audit report AR-00-OUTAG-01, dated July 7, 2000, stated, in part, Boric

Acid Corrosion Control Checklists and Condition Reports were initiated by

inspectors when prudent to document and evaluate boric acid accumulation and

leaks. Boric acid leakage was adequately classified and corrected when

appropriate. Engineering displayed noteworthy persistence in ensuring boric

acid accumulation from the reactor head was thoroughly cleaned. This audit

report contains inaccurate information: (1) the reactor head was not thoroughly

18

cleaned during the outage; (2) a boric acid corrosion control checklist was not

prepared for the boric acid left on the head after the cleaning attempt; and (3)

the boric acid accumulation and leaks were not identified, properly classified, nor

corrected.

8.

Davis-Besse letter, Serial 2731, September 4, 2001, Response to

Bulletin 2001-01, contained the following four inaccuracies:

a.

The response to Item 1.c on page 2 of 19 contained the statement that

the minimum gap being at the dome center of the RPV head where it is

approximately 2 inches, and does not impede a qualified visual

inspection. This is contradicted by statements in several PCAQRs, most

notably 94-0295, which prompted the reintroduction of the service

structure modification, and 96-0551 which clearly stated that inspection

capability at the top of the head was limited. This limitation was caused

by the restricted access to the area through the service structure weep

holes, the curvature of the reactor pressure vessel head, and by the

limited space to manipulate a camera due to the insulation that creates

the two inch gap.

b.

Item 1.d of the Bulletin directed inclusion of a description of any

limitations (insulation or other impediments) to accessibility of the bare

metal of the RPV head for visual examinations. The response was

incomplete in that it did not mention that accessibility to the bare metal of

the reactor head was impeded by the significant accumulations of boric

acid deposits in both the eleventh and twelfth RFOs.

c.

Item 1.d of the bulletin directed a discussion of the findings of vessel

head inspections. The response to this on page 3 for the twelfth RFO

was that inspection of the RPV head/nozzles indicated some

accumulation of boric acid deposits. This was a mischaracterization of

the accumulations as evidenced by the pictures and the video

examination of conditions on the head at the beginning and ending of the

outage.

d.

Additionally on page 3, the response stated, The boric acid deposits

were located beneath the leaking flanges with clear evidence of

downward flow. No visible evidence of nozzle leakage was detected.

This was inaccurate, in that the boric acid deposits were not all located

under leaking flanges and there was no clear evidence of downward flow

for all nozzles. The deposits were not limited to the area beneath the

flanges as implied by that statement and, in fact, the build-up was so

significant that all of the nozzles could not be inspected. There was no

basis for stating that no visible evidence of nozzle leakage was detected.

9.

Davis-Besse letter, Serial 2735, October 17, 2001, Supplemental Response to

Bulletin 2001-01, stated, In May 1996, during a refueling outage, the RPV head

was inspected. No leakage was identified, and these results have been recently

verified by a re-review of the video tapes obtained from that inspection. The

19

RPV head was mechanically cleaned at the end of the outage. Subsequent

inspections of the RPV head in the next two refueling outages (1998 and 2000),

also did not identify any leakage in the CRDM nozzle-to-head areas that could

be inspected. Video tapes taken during these inspections have also been

re-reviewed. These statements were inaccurate in that they implied that the

head was completely cleaned and inspected. The RPV head could not be

completely inspected, as evidenced by PCAQR 96-0551. The RPV head was

not cleaned as evidenced by PCAQR prepared at the start of the 1998 outage

which stated that there were old boric acid deposits on the head.

c.

Analysis

This issue represented a licensee performance deficiency. Completeness and accuracy

of information are essential to the ability of the USNRC to establish a regulatory position

on issues which can affect the health and safety of the general public. Completeness

and accuracy in the documents listed above may have provided an earlier alert to the

licensee staff and the USNRC about the problems with CRDM nozzle leakage or may

have caused the USNRC to establish a different regulatory position concerning the

urgency of inspections for the RPV head. Consequently, this was considered a finding

of more than minor safety significance because the cavity in the reactor vessel head

represented a loss of the design basis barrier integrity.

d.

Enforcement

10 CFR 50.9 requires that information provided to the Commission by a licensee or

information required by statute or by the Commissions regulations, order, or license

conditions maintained by the licensee shall be complete and accurate in all material

respects. The examples listed contain incomplete or inaccurate information material to

the USNRC. The significance of these examples requires additional review as specified

in NUREG-1600, General Statement of Policy and Procedures for USNRC

Enforcement. Because the safety significance of the apparent violation has yet to be

determined, the issue will be classified as an unresolved item and will be identified as

URI 50-346/02-08-10, Completeness and Accuracy of Information.

4OA6 Management Meetings

Exit Meeting Summary

The inspectors presented the inspection results to Mr. L. Myers and other members of

licensee management and staff at the conclusion of the inspection on August 9, 2002.

The licensee acknowledged the information presented. Proprietary information

reviewed and retained by the inspectors was identified.

20

KEY POINTS OF CONTACT

DAVIS-BESSE

D. Baker, LCM(A) Manager

R. Fast, Plant Manager

J. Grabnar, Design Basis Engineering Manager

D. Gudger, Learning Organization Manager

D. Haskins, Human Resources Manager

S. Loehlein, Principal Nuclear Consultant

L. Myers, Site Vice President

L. Pearce, Vice President, Oversight

J. Powers, Engineering Director

P. Roberts, Maintenance Manager

M. Roder, Operations Manager

J. Rogers, Plant Engineering Manager

R. Slyker, Licensing Staff Engineer

H. Stevens, Quality Assurance Manager

G. Wolf, Licensing Staff Engineer

NUCLEAR REGULATORY COMMISSION

J. Grobe, Chairman, Davis-Besse Oversight Panel

C. Lipa, Chief, Reactor Projects Branch 4

S. Thomas, Senior Resident Inspector

LIST OF ACRONYMS USED

AIT

Augmented Inspection Team

ASME

American Society of Mechanical Engineers

B&W

Babcock and Wilcox

CAC

Containment Air Cooler

CR

Condition Report

CRDM

Control Rod Drive Mechanism

EPRI

Electric Power Research Institute

GL

Generic Letter

gpm

Gallon Per Minute

LOCA

Loss of Coolant Accident

PCAQR

Potential Conditions Adverse to Quality Report

PDR

Public Document Room

RCS

Reactor Coolant System

RE

Radiation Element

RFO

Refueling Outage

RPV

Reactor Pressure Vessel

SDP

Significance Determination Process

URI

Unresolved Item

USNRC

U. S. Nuclear Regulatory Commission

21

ITEMS OPENED

50-346/2002-08-01

URI

Reactor Operation with Pressure Boundary Leakage

50-346/2002-08-02

URI

Reactor Vessel Head Boric Acid Deposits

50-346/2002-08-03

URI

Containment Air Cooler Boric Acid Deposits

50-346/2002-08-04

URI

Radiation Element Filters

50-346/2002-08-05

URI

Service Structure Modification Delay

50-346/2002-08-06

URI

Reactor Coolant System Unidentified Leakage Trend

50-346/2002-08-07

URI

Inadequate Boric Acid Corrosion Control Program

Procedure

50-346/2002-08-08

URI

Failure to Follow Boric Acid Corrosion Control Program

Procedure

50-346/2002-08-09

URI

Failure to Follow Corrective Action Program Procedure

50-346/2002-08-10

URI

Completeness and Accuracy of Information

22

LIST OF DOCUMENTS REVIEWED

The following is a list of licensee documents reviewed during the inspection, including

documents prepared by others for the licensee. Inclusion on this list does not imply that

USNRC inspectors reviewed the documents in their entirety, but, rather that selected sections

or portions of the documents were evaluated as part of the overall inspection effort. Inclusion

on this list does not imply USNRC acceptance of the document, unless specifically stated in the

inspection report.

Procedures

NG-EN-00324

Boric Acid Corrosion Control, Revisions 1, 2, and 3

NG-NA-00305

Operating Experience Program

NG-NA-00702

Corrective Action Program, Revision 3

DB-PF-00204

ASME Section XI Pressure Testing, Revision 3

DB-OP-01200

Reactor Coolant System Leakage Management, Revision 3

Potential Conditions Adverse to Quality Reports (PCAQR)

1991-0353

Boron on Reactor Vessel Head

1992-0072

CAC Cleaning

1993-0132

Reactor Coolant Leakage from CRD Flange

1994-0295

Improper Closure of the Nozzle Leakage Inspection Commitment

1994-0912

Documents Results of CRDM leakage Video Inspection

1996-0551

Boric Acid on RX Vessel Head

1996-0650

VT-2 Inspection Revealed Evidence of Leakage and Boric Acid Residue

1998-0649

Reactor Vessel Head Boron Deposits

1998-0767

Reactor Vessel Head Inspection Results

1998-0824

CAC Boric Acid Accumulation

1998-1164

Water in RE4597 Sample Lines

1998-1895

CTMT Normal Sump Leakage in Excess of 1 gpm

1998-1965

Water and Boron Accumulation on Filter Cartridges

1998-1980

Potential CAC Fouling

1998-2071

Accumulation of Boric Acid on CTMT Service Water Piping

Condition Reports (CR)

1992-0139

Boron Found on Containment Air Sample Filter

1993-0187

Boric Acid Accumulation on SW Piping

1999-0372

Received Computer PT-RE4597AA/AB High

1999-0510

Low Flow Alarm Observed on RE4597BA While Out of Service for Maintenance

1999-0745

Small Clumps of Boric Acid Present on Wall Opposite of DH108

1999-0861

RE4597AA Sample Lines Were Found to be Full of Water

1999-0928

Increased Frequency of Particulate and Charcoal Filters for RE 4597BA Being

Changed

1999-1300

Analysis of CTMT Radiation Monitor Filters

1999-1614

Due Date of LER Commitment Missed: Boric Acid Control Program Procedure

Change

23

2000-0781

Leakage from CRD Structure Blocked Visual Exam of Reactor Vessel Head

Studs

2000-0782

Inspection of Reactor Flange Indicated Boric Acid Leakage From Weep Holes

2000-0994

RV Head CRDM Nozzle at Location F-10 has Large Pit in Outer Gasket Groove

2000-0995

RV Head CRDM Nozzle Flange at Location D-10 has Extensive Pitting Across

the Outer Gasket Groove. Inner Gasket Also Has Pitting

2000-1037

Inspection of Reactor Head Indicated Accumulation of Boron in Area of the CRD

Nozzle Penetration

2000-1547

CAC Plennum Pressure Drop Following 12 RFO

2000-4138

Frequency for Cleaning Boron From CAC Fins Increased to Interval of

Approximately 8 Weeks

2001-0039

CAC Plenum Pressure Experienced Step Drop

2001-0890

Unidentified RCS Leak Rate Varies Daily by as Much as 100 percent of the

Value

2001-1110

Chemistry is Changing Filters on RE4597BA More Frequently

2001-1822

Frequency of Filter Changes for RE4597BA is Increasing

2001-1857

RCS Unidentified Leakage at .125 to .145 gpm

2001-2769

RE2387 Identified Spiked Above ALERT and High Setpoints

2001-2795

RE4597BA Alarmed on Saturation

2001-2862

Calculated Unidentified Leakage for Reactor Coolant System has Indicated

Increasing Trend

2001-3025

Increase in RCS Unidentified Leakage

2001-3411

Received Equipment Fail Alarm for Detector Saturation on RE4597BA

2002-0685

Loose Boron 1-2" deep 75% Around Circumference of Flange

2002-0846

More Boron Than Expected Found on Top of Head

Modifications

MOD 90-0012

Modification Reactor Closure Head Access Ports

MOD 94-0025

Install Service Structure Inspection Openings

USNRC Generic Communications for Control of Boric Acid Corrosion

IN 86-108

Degradation of Reactor Coolant System Pressure Boundary Resulting

from Boric Acid Corrosion, December 29, 1986

IN 86-108

Supplement 1, April 20,1987

IN 86-108

Supplement 2, November 19, 1987

IN 86-108

Supplement 3, January 5, 1995

GL 88-05

Boric Acid Corrosion of Carbon Steel Reactor Pressure Boundary

Components in PWR Plants, March,17, 1988

IN 90-10

Primary Water Stress Corrosion Cracking (PWSCC) of Inconel 600,

February 23,1990

IN 94-63

Boric Acid Corrosion of Charging Pump Casing Caused by Cladding

Cracks, August 30, 1994

IN 96-11

Ingress of Demineralizer Resins Increases Potential for Stress Corrosion

Cracking of Control Rod Drive Mechanism Penetrations,

February 14,1996

GL 97-01

Degradation of CRDM/CEDM Nozzle and other Vessel Closure Head

Penetrations, April 1, 1997

24

IN 2001-05

Through-wall Circumferential Cracks of Reactor Pressure Vessel Head

Control Rod Drive Mechanism Penetration Nozzles at Oconee Nuclear

Station, Unit 3, April 30, 2001

Bulletin 2001-01

Circumferential Cracking of Reactor Pressure Vessel Head Penetration

Nozzles, dated August 3, 2001

Other Documents

RAS02-00132

Probable Cause Summary Report for CR2002-0891, March 22, 2002

BAW-10190P

Safety Evaluation For B&W Design Reactor Vessel Head Control Rod

Drive Mechanism Nozzle Cracking, May 1993

BAW-10190P,

Addendum 1

B&W Owners Group Proprietary, External Circumferential Crack Growth

Analysis for B&W-Design Reactor Vessel Head Control Rod Drive

Mechanism Nozzle Cracking, December 1993

BAW-10190P,

Addendum 2,

B&W Owners Group Proprietary, Safety Evaluation for Control Rod Drive

Mechanism Nozzle J-Groove Weld

BAW-2301

B&W Owners Group Proprietary, B&WOG Integrated Response to

Generic Letter 97-01, July 1997

Framatome

51-5015818-00

Davis-Besse CRDM Nozzle Heat Information, 2002

51-125825-00

CRDM Nozzle Heat Treatment

51-1218440-00

Alloy PWSCC Time-to-Failure Models

51-1219143-00

CRDM Nozzle Characterization

51-1219275-01

CRDM Leakage Detection Evaluation

51-1229638-00

Boric Acid Corrosion Data Summary and Evaluation

51-1201160-00

Alloy 600 SCC Susceptibility: Scoping Study of Components at Crystal

River 3

Memorandum

Control Rod Drive Nozzle Cracking, May 8, 1996

Root Cause Plan

Dated March 18, 2002.

Intra-Company

Memorandum

Probable Cause Summary Report for CR2002-0891, March 22, 2002

Meeting Minutes

DBPRC Meeting Minutes for MOD 94-0025.

WO 00-001846-00

Work Order - Clean Reactor Head

AR-00-OUTAG-01

QA Audit Report Refueling Outage 12

Serial 2472

Davis-Besse Letter: Response to Generic Letter 97-01, July 28, 1997

Serial 2731

Davis-Besse Letter: Response to Bulletin 2001-01, September 4, 2001

Serial 2735

Davis-Besse Letter: Supplemental Response to Bulletin 2001-01, October

17, 2001

ASME

ASME Boiler and Pressure Vessel Code,Section XI, 1986

Edition and 1995 Edition with 1996 Addenda

25

Photographic Records

Video Tape

Davis-Besse Reactor Head Inspection Under Insulation Alloy 600, 12 RFO

Video Tape

Davis-Besse 12 RFO Final Head Inspection

Video Tape

Davis-Besse Reactor Head Cleaning 11 RFO

Video Tape

Davis-Besse Weep Hole Cleaning Nozzle 67, 10 RFO

Video Tape

Davis-Besse Weep Hole Video Inspection 10 RFO

Video Tape

13 RFO Reactor Head Nozzle Remote Visual Inspection

Video Tape

Root Cause Video of Nozzle #3 and Adjacent Nozzles, March 13, 2002 to

March 14, 2002

Video Tape

PT of Nozzle #46 J-groove Weld, March 24, 2002