ML021350673

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IR 05000387/2002-301 and IR 05000388/2002-301, Hope Creek Station, Inspection on March 11-18, 2002, Related to Initial Operator Licensing Examinations. Four of Five Reactor Operator Applicants Passed All Portions of the Examination
ML021350673
Person / Time
Site: Hope Creek PSEG icon.png
Issue date: 05/15/2002
From: Conte R
Division of Nuclear Materials Safety I
To: Keiser H
Public Service Enterprise Group
Shared Package
ML012980106 List:
References
05000354/2002-301 IR-02-301
Download: ML021350673 (22)


See also: IR 05000387/2002301

Text

May 15, 2002

Mr. Harold W. Keiser

Chief Nuclear Officer and President

PSEG Nuclear LLC - N09

P.O. Box 236

Hancocks Bridge, NJ 08038

SUBJECT: HOPE CREEK GENERATING STATION REACTOR OPERATOR AND SENIOR

REACTOR OPERATOR INITIAL EXAMINATION REPORT NO. 50-354/02-301

Dear Mr. Keiser:

This report transmits the results of the reactor operator and senior reactor operator licensing

examinations conducted by the NRC during the period of March 11-18, 2002. These

examinations addressed areas important to public health and safety and were developed and

administered using the guidelines of the Examination Standards for Power Reactors

(NUREG-1021, Revision 8).

Based on the results of the examination, all three Senior Reactor Operator and four of five

Reactor Operator applicants passed all portions of the examination. One Reactor Operator

applicant failed the administrative section of the examination. Performance insights observed

during the examination process were discussed between Mr. DAntonio and training personnel

on March 15, 2002. Results of the examinations were given to training department

management on April 4, 2002.

There were a large number of changes to the written exam after it was administered - eight

deletions for the RO test and four deletions for the SRO test, and three other answer key

changes on both the RO and SRO examination, two of which involved questions with two

correct answers. Overall this resulted in deleting or changing the answers for 11% of the RO

test and 7% of the SRO test. Because many of the changes (>5%) were related to site specific

information, this problem indicated preliminarily a poor quality of review by your staff. The

region verified no impact on the written test outline sampling plan. However, in accordance with

Examination Standards (NUREG-1021), Section ES-501, item C.2.c., we request a response to

this letter in which you provide your perspective on the problem, including why so many

changes were necessary and what actions, if any, have been taken or will be taken to improve

future initial licensing examinations.

In accordance with 10 CFR 2.790 of the NRC's "Rules of Practice," a copy of this letter and its

enclosure will be available electronically for public inspection in the NRC Public Document

Mr. Harold W. Keiser -2-

Room or from the Publicly Available Records (PARS) component of NRCs document system

(ADAMS). These records which include the final examinations are available in ADAMS

(RO/SRO Written-Accession No. ML021350097; RO/SRO Operating Section A-Accession

No. ML021080751; RO/SRO Operating Section B- Accession No. ML021090019 and

ML021350127; RO/SRO Operating Section C-Accession No. ML021090041; Facility Post

Examination Comments on the Written Exams - Accession No. ML021350211. ADAMS is

accessible from the NRC Web site at http://www.nrc.gov/reading-rm/ADAMS.html (the Public

Electronic Reading Room).

Sincerely,

/RA/

Richard J. Conte, Chief

Operational Safety Branch

Division of Reactor Safety

Docket No: 50-354

License No: NPF-57

Enclosure: Examination Report 50-354/2002-301 with Attachment 1

cc w/encl; w/Attachment 1:

D. Jackson, Manager - Operations Training

cc w/encl w/o Attachment 1:

E. Simpson, Senior Vice President and Chief Administrative Officer

M. Bezilla, Vice President - Technical support

D. Garchow, Vice President - Operations

G. Salamon, Manager - Licensing

R. Kankus, Joint Owner Affairs

J. J. Keenan, Esquire

Consumer Advocate, Office of Consumer Advocate

F. Pompper, Chief of Police and Emergency Management Coordinator

M. Wetterhahn, Esquire

N. Cohen, Coordinator - Unplug Salem Campaign

E. Gbur, Coordinator - Jersey Shore Nuclear Watch

E. Zobian, Coordinator - Jersey Shore Anti Nuclear Alliance

State of New Jersey

State of Delaware

Mr. Harold W. Keiser -3-

Distribution w/encl; w/o Attachment 1:

Region I Docket Room (with concurrences)

J. Schoppy - NRC Resident Inspector

H. Miller, RA/J. Wiggins, DRA

G. Meyer, DRP

R. Barkley, DRP

T. Haverkamp, DRP

L. Prividy, DRS

T. Bergman, OEDO

S. Richards, NRR

G. Wunder, PM, NRR

R. Fretz, Backup PM, NRR

W. Lanning, DRS

J. DAntonio, Chief Examiner, DRS

C. Buracker, DRS

DRS File

DOCUMENT NAME:C:\ORPCheckout\FileNET\ML021350673.wpd

ADAMS Package No.: ML012980106

After declaring this document An Official Agency Record it will be released to the Public.

To receive a copy of this document, indicate in the box: "C" = Copy without attachment/enclosure "E" = Copy with attachment/enclosure "N" = No copy

OFFICE RI/DRS RI/DRP RI/DRS

NAME JDAntonio GMeyer RConte

DATE 04/ /02 05/ /02 05/ /02 05/ /02 05/ /02

OFFICIAL RECORD COPY

U.S. NUCLEAR REGULATORY COMMISSION

REGION I

Docket No. 50-354

License No. NPF-57

Report No. 50-354/2002-301

Licensee: PSEG Nuclear LLC - N09

Facility: Hope Creek Nuclear Generating Station

Location: Hancocks Bridge, New Jersey

Dates: March 11-18, 2002 (Operating and Written Exam Administration)

March 26-April 3, 2002 (Grading)

Examiners: J. DAntonio, Operations Engineer (Chief Examiner)

T. Fish, Operations Engineer

C. Sisco, Operations Engineer

Approved by: Richard J. Conte, Chief

Operational Safety Branch

Division of Reactor Safety

SUMMARY OF FINDINGS

IR 05000387/2002-301 and 05000388/2002-301; March 11-18, 2002; PSEG Nuclear LLC -

N09; Hope Creek Generating Station; Initial Operator Licensing Examinations.

The inspection was conducted by three regional operator licensing examiners.

Cornerstone: Mitigating Systems

Three of three SRO and four of five RO applicants passed all portions of the

examinations. The written examinations were administered by the facility and the

operating tests were administered by three NRC examiners. Because of the relatively

large number of post exam changes to the written exam (in excess of 5%), the quality of

the initial submital was considered problematic.

-ii-

Report Details

1. REACTOR SAFETY

Mitigating Systems

Reactor and Senior Reactor Operator Initial Licensing Examination

a. Scope

The NRC examination team reviewed the written and operating examinations and post

exam materials submitted by the Susquehanna training staff to verify or ensure, as

applicable, the following:

 The examinations were developed in accordance with the guidelines of Revision

8 of NUREG-1021, "Operator Licensing Examination Standards for Power

Reactors and they met the overall quality goals (range of acceptability) of these

standards. The review was conducted both in the Region I office and at the

Susquehanna training facility. Final resolution of comments and incorporation of

test revisions were made during and following the onsite preparation week.

 Simulation facility operation was proper.

 Facility licensee completed a test item analysis on the written exams for

feedback into the systems approach to training program.

 Examination security requirements were met.

The NRC examiners administered the operating portion of the exams to all applicants on

March 11-15, 2002. Hope Creek training staff administered the written examinations on

March 18, 2002.

 Findings

Grading and Results:

Three of three SRO and four of five RO Applicants passed all portions of the

examinations.

Examination Preparation and Quality:

During the pre-exam NRC review, the exam did not exceed the quality tolerances of the

examiners standards. After the examination, the facility had twelve (12) post-

examination comments on the written exam - eight deletions for the RO test and four

deletions for the SRO test, and three other answer key changes on both the RO and

SRO examination two of which involved questions with two correct answers. Overall this

resulted in deleting or changing the answers for 11% of the RO test and 7% of the SRO

test. This was a relatively large number of changes to the written exam (in excess of

2

5% ) of the total questions submitted for the RO and SRO exams. The NRC accepted

ten facility comments, denied one deletion, and deleted one question for which the

facility requested an answer key change. A summary of facility comments on the written

test and NRC resolution is attached to this report.

The facility also requested modification of the critical task standard for one

administrative JPM. No change to the critical task standard for the administrative JPM

occurred as addressed below.

The licensee request that the task standard for JPM RO-A.4 be modified. The

requirement to circle LPCI flow to indicate the plant is in other than LPCI injection mode

is not critical for several reasons:

 Plant pressure is too high for the indicated LPCI flow to be injection flow.

 Plant pressure elevated 20 min after a LOCA indicates a very small LOCA.

 RPV level is being maintained with normal feed and condensate.

 If the operator had circled LPCI flow, additional information would still be

necessary.

 The personnel receiving this status sheet are knowledgeable and would not be

confused about plant status by the absence of the circle indicating LPCI not in

injection mode.

 There were a number of items for the applicant to check in this JPM, circling

RHR flow is a small part of the total task.

The facility indicated that locating the appropriate instrumentation to validate the status

board sheet was the critical aspect of this JPM; failing to indicate LPCI mode was a

minor omission of no safety consequence.

The NRC staff did not accept the comment. The requirement to identify RHR not in

LPCI mode was the only aspect of this JPM that was something other than a

verification. If not circled, it could have misled the recipients of the information, i.e., the

Technical Support Center (TSC) on actual status of LPCI mode during an emergency

resulting in misinformation on unnecessary additional communications. The applicant or

operator has the responsibility to pay attention to all procedural details and provide

accurate information whether or not LPCI was actually injecting, the adequacy of the

data sheet, or the ability of personnel outside the control room to deduce actual plant

status from other information on the sheet, For future use the JPM should be enhanced

in order to have the applicant or operator demonstrate the ability to find and record

accurate data and clearly indicate in the JPM the end point of the task, e.g., applicant or

operator ready to send the information to the TSC.

Examination Administration and Performance:

No findings of significance were identified

4.0 OTHER ACTIVITIES

3

4OA6 Meetings, including Exit

On March 15, 2002 the NRC provided observations associated with the exam to Hope

Creek training personnel. Examination results were provided to the facility on April 4,

2002. License numbers were also provided during the April 4 telephone call.

The NRC expressed appreciation for the cooperation and assistance that was provided

during the preparation and administration of the exams by the licensees training and

operation staffs.

4

KEY POINTS OF CONTACT

Licensee

Jim Reid........................................Manager, Nuclear Operations Training

Nick Conicella................................Operations Superintendent - Hope Creek Licensed Training

Archie Faulkner..............................NRC Exam Development Supervisor

LIST OF ITEMS OPENED, CLOSED, AND DISCUSSED

ITEM NUMBER TYPE DESCRIPTION

NONE

Summary of Hope Creek Requested Changes and NRC Resolution

Exa RO/S Facilit Facility Facility Facility Comment

m RO y Rec.: Rec.:

Rec Quest Rec.: Two Change

ord ion Delete correct Answer

No. No. / answer

Reaso s

n

4 4/- No Delete question. No correct answer. Answer

Correc choice "C" does not limit flow to only

t "system" flow. HC.OP-SO.BC-0002 step

Answe

5.2.31 and 5.2.33 allow throttling flow with

r

F003A(B) which are NOT affected by the

stated bus loss. Also, as stated in Caution

5.2.31 and 5.2.33, the F003A(B) may be used

to throttle flow through the heat exchanger.

System flow is normally established with the

F015A(B). In the question, both F015 A and B

valves lose power from the 10A404 bus loss.

NRC Resolution: Delete question due to no correct answer

The NRC requested and reviewed the following additional material - related RHR system

prints and electrical prints showing power supplies to valves F003A(B). The question asks

the applicant to identify the effect on Shutdown Cooling flow for a given electrical bus loss.

The examiner verified that the bus loss does not affect F003A(B) and as such the condition

does not result in the loss of ability to adjust flow as stated in answer C. Therefore there is

no correct answer.

Based on the above review, the NRC staff accepted the facility comment.

2

Exa RO/S Facilit Facility Facility Facility Comment

m RO y Rec.: Rec.:

Rec Quest Rec.: Two Change

ord ion Delete correct Answer

No. No. / answer

Reaso s

n

13 11/12 X Recommend accept 2 correct answers B and

D. The Technical Specification Bases 3/4 3.9

supports answer B, which states the reason for

the high RPV Level Main Turbine trip is to

prevent Main Turbine damage. The bases is

brief and does not contain detailed discussion

of the high level trip. Lesson Plan 0301-

000.00H-000002-15 page 13 and 14 supports

answer choice D which states HPCI, RCIC,

and Reactor Feed Pumps are tripped to prevent

RPV overfill and flooding the main steam

lines, then states the significant safety concerns

if overfill occurred including "Stressing of the

reactor main steam line nozzles, steam line

snubbers, pipe supports and hangers as a result

of: - The weight of water in the main steam

lines; and the dynamic transient loads caused

by water flow in the main steam lines." This is

further supported by NRC INFO NOTICE 88-

77, which is also referenced in the lesson plan

and addresses RPV overfill and flooding the

main steam lines. This is further supported by

the bases in Improved Standard Technical

Specifications.

NRC Resolution: Change answer key to accept two correct answers

The examiner reviewed the Technical Specifications and applicable lesson plans submitted

by the facility and verified that answer choices B and D are reasons for the automatic trip

of the reactor feedwater pumps on increasing reactor water level for a malfunction of the

Digital Feedwater System.

Based on the above review, the NRC staff accepted the facility comment.

3

Exa RO/S Facilit Facility Facility Facility Comment

m RO y Rec.: Rec.:

Rec Quest Rec.: Two Change

ord ion Delete correct Answer

No. No. / answer

Reaso s

n

31 21/28 X Recommend Answer Key change from B to

D. Upon trip of the CRD Pump, HCU

Accumulator charging water check valves

(V115) begin leaking through the valve seats,

causing the accumulator pistons to move. The

N2 gas pressure lowers when the accumulator

piston moves. (See P&ID M-47 Sheet 1) The

surveillance requirements of HC.OP-IS.BF-

0103 demonstrate the leakage rate is low

enough to prevent accumulator trouble alarms

for greater than 2 minutes. The accumulator

alarms when nitrogen gas side pressure lowers

to 940 psig. The original assumption was that

there was no leakage past the check valves,

however, as stated previously there is some

leakage past the check valves that would affect

gas pressure and cause it to lower.

NRC Resolution: Change answer key from B to D

The NRC requested and reviewed additional material - copy of last completed surveillance

accumulator surveillance. There was evidence of leakage based on actual plant conditions

making answer choice D the correct answer based on actual plant conditions.

Based on above review, the NRC staff accepted the facility comment.

4

Exa RO/S Facilit Facility Facility Facility Comment

m RO y Rec.: Rec.:

Rec Quest Rec.: Two Change

ord ion Delete correct Answer

No. No. / answer

Reaso s

n

46 34/- Level Delete question. RO candidates were not

of provided the HC Event Classification Guide to

Difficul correlate the ALERT level EOP 103/4 entry

ty

condition to a radiation level. ECG Section 6.1

provides that correlation. Without the ECG, the

question becomes a Level of Difficulty 5

memory question relying on memory of

wording contained in Lesson Plan 0302-

000.00H-000127-12. The text for Learning

Objective 2 states: "The entry condition for

Radioactivity Release Control corresponds to

an action level defined in the site Emergency

Plan."

ECG Bases document states that the ECG

Initiating Condition is entered when

radioactive release rates reach levels

corresponding to 200 times 10CFR20,

Appendix B Limits. These levels are high

enough that they will not occur during normal

operation, but still low enough that the

immediate health and safety of the general

public is not threatened by the release."

NRC Resolution: Delete question due to excessive difficulty

The NRC requested and reviewed additional material - RO lesson plan showing lesson

objectives regarding expected RO knowledge of ECG classifications. Accordingly it was

overly difficult for the RO applicants to answer this question without the ECG classification

guide.

Based on review, the NRC staff accepted the facility comment.

5

Exa RO/S Facilit Facility Facility Facility Comment

m RO y Rec.: Rec.:

Rec Quest Rec.: Two Change

ord ion Delete correct Answer

No. No. / answer

Reaso s

n

48 36/43 *X Recommend Answer Key change to D.

The Hydrogen alarms are set to alarm at 2.0%

Hydrogen concentration on the H2/O2

Analyzers. Conditions provided in the stem

indicate the reactor core would be degraded

and producing hydrogen. EOP 102 Step

PC/H3 directs the Hydrogen Recombiners to

be placed in service if H2 concentration

reaches 0.5%. Placing the H2 Recombiners in

service IAW step PC/H3 would be the required

action. (Answer D)

Hydrogen alarms are clear indicating

Hydrogen Concentration is less than 2.0%,

therefore, EXIT EOP 102 and enter SAG is

not required. (Answer B)

NRC Resolution: *Facility recommendation changed to delete question due to no correct

answer

The NRC reviewed the applicable EOP and determined that this question cannot be

answered. The question stem does not give enough information about H2 concentration,

therefore applicants cannot determine that H2 >.5% to select the proposed answer.

Based on the above review, the NRC staff did not accepted the facility comment in part.

6

Exa RO/S Facilit Facility Facility Facility Comment

m RO y Rec.: Rec.:

Rec Quest Rec.: Two Change

ord ion Delete correct Answer

No. No. / answer

Reaso s

n

68 55/- Level Delete question. Level of Difficulty 5. The

of question requires memorization of the

Difficul prerequisite 2.6.2 of HC.OP-SO.SB-0001. The

ty

procedure should have been referenced in the

question.

NRC Resolution: Delete question due to excessive difficulty

The NRC requested and reviewed additional material - Reactor Protection System lesson

plan, full copy of SB-001 and

Problem Report referenced in note at step 5.6. This question requires knowledge of a note

at step 5.6 of the procedure SB-001 rather than the prerequisites as to when the reactor

mode switch shutdown position scram may be bypassed. This particular knowledge item is

not addressed in the lesson objectives or the lesson plan.

Based on the above review, the NRC staff accepted the facility comment.

7

Exa RO/S Facilit Facility Facility Facility Comment

m RO y Rec.: Rec.:

Rec Quest Rec.: Two Change

ord ion Delete correct Answer

No. No. / answer

Reaso s

n

73 59/60 No Delete question. No correct answer.

Correc LPRM 32-33-C is assigned to LPRM Group A

t IAW HC.RE-ST.SE-0003 Attachment 1. All

Answe

answer choices affect an APRM. The answer

r

would have been correct if the LPRM chosen

belonged to APRM C or D. Additionally, the

candidates were not given a reference to

determine which APRM the LPRM was

assigned. The readings of the LPRM and

APRM before the failure occurred would also

be necessary to determine if the average went

up or down after the failure.

NRC Resolution: Delete the question due to no correct answer.

The examiner verified that this question references a specific LPRM which does not provide

an input to the APRMs.

Based on the above review, the NRC accepted the facility comment.

8

Exa RO/S Facilit Facility Facility Facility Comment

m RO y Rec.: Rec.:

Rec Quest Rec.: Two Change

ord ion Delete correct Answer

No. No. / answer

Reaso s

n

106 87/83 *No Delete question. No correct answer.

Correc Immediate Operator Action of HC.OP-AB.ZZ-

t 0129 3.1 states "If smoke OR toxic gases are

Answe

detected in the control room air supply, isolate

r

the Control Room ventilation and place CREF

in the RECIRC MODE" . Keyed answer D

contains part of that answer. Pressing the

Control room EMER FILTER UNIT A and B

RECIRC MODE pushbuttons alone will not

start CREF or place CREF in the RECIRC

MODE. CREF must be running for the Recirc

Dampers to open.

NRC Resolution: * No change to the answer key

The NRC requested and reviewed additional material - Operating procedure to isolate CR

ventilation and place CREF in RECIRC. The question asks for AN immediate action; the

fact that the abnormal procedure specifies two actions in one sentence and the key answer is

not the first of those actions does not invalidate the question.

Based on the above review, the NRC staff did not accept this comment.

9

Exa RO/S Facilit Facility Facility Facility Comment

m RO y Rec.: Rec.:

Rec Quest Rec.: Two Change

ord ion Delete correct Answer

No. No. / answer

Reaso s

n

116 92/- No Delete question. No Correct answer. IAW

Correc NC.NA-AP.ZZ-0049, Definitions 7.2. "Formal

t declaration of Suspension of Core Alterations

Answe

or Fuel Handling is performed by the

r

Refueling SRO or a condition required by

Technical Specifications." None of the answer

choices contained conditions required by

Technical Specifications that would require

Suspension of Core Alterations.

Additionally, Lesson Plan 302-000-00H-

000113-10 Obj 66 states< "Determine the

conditions under which handling of fuel must

be suspended, IAW NC.NA-AP.ZZ-0049.

(SRO ONLY)". Therefore the question is not

appropriate

NRC Resolution: Delete due to no correct answer

The NRC requested and reviewed additional material - Refueling Operations procedure, and

administrative lesson plan addressing responsibility for suspension of fuel handling

operations. The examiner verified there was no correct answer.

Based on the above review, the NRC accepted the facility comment.

10

Exa RO/S Facilit Facility Facility Facility Comment

m RO y Rec.: Rec.:

Rec Quest Rec.: Two Change

ord ion Delete correct Answer

No. No. / answer

Reaso s

n

120 94/93 No Delete question for four candidates due to question

Correc contained a typographical error that allowed no correct

answer choice. These 4 students had completed and

t turned in their exams prior to the discovery of the error.

Answe The error was in the stem, Entry 2, Neutron dose should

r have read 24 instead of 54 mrem. Calculating the

for answer based on the error resulted in a remaining dose

of 1491 mrem. (Reference NC.NA-AP.ZZ-0024)

Four Previous history TEDE = DDE + CEDE; TEDE = 210 +

Applic 45; TEDE = 255 mrem

ants Todays dose: Gamma dose + Neutron dose Entry 1 +

Gamma dose + Neutron dose Entry 2 = DDE

Entry 1 = (52 + 24) + Entry 2 = (124 + 54)

Typo Todays dose = 76 + 178 = 254 mrem

Fixed Remaining dose = Admin limit (2000 mrem TEDE) -

for Previous history (255 mrem) - todays dose (254 mrem)

Four Remaining dose = 1491 mrem

The closest answers were A: 1488 mrem and B: 1521

Applic mrem, both of which are incorrect for the question

ants asked.

Once the error was identified, it was made known to the

4 remaining candidates. The correction was then written

on the board. The question will remain valid for these 4

candidates.

NRC Resolution: Answer key unchanged for 4 applicants who were made aware of the

typographical error in the stem of the question and question deleted for

other applicants who were not aware of the typographical error in the

stem of the question

The NRC verified exam completion times for the applicants who were not made aware of the

typographical error to ensure this question would be deleted only for those applicants who

had left prior to correction of the error,

Based on the above review, the NRC staff accepted the facility comment.

11

Exa RO/S Facilit Facility Facility Facility Comment

m RO y Rec.: Rec.:

Rec Quest Rec.: Two Change

ord ion Delete correct Answer

No. No. / answer

Reaso s

n

126 98/97 X Recommend accept 2 correct answers A

and C. SH.OP-AP.ZZ-0102 step 5.5.2

supports answer C. However, there are

numerous 100 series Abnormal procedures

that are operational transients. Abnormal

procedures HC.OP-AB.ZZ-0138 Main Turbine

Trip and HC.OP-AB.ZZ-0110 Loss of an RPS

Channel are examples of operational

transients. Answer A stated 100 series are

operational transient procedures which is

technically correct.

There is currently a major effort underway to

correct identified deficiencies to enhance

these procedures and governing documents.

NRC Resolution: Change answer key to accept two correct answers

The NRC requested and reviewed additional material - Procedure index for 100 series

procedures. The examiner verified that various 100 and 200 series procedures address

events which are normally considered operational transients.

Based on the above review, the NRC staff accepted the facility comment.

12

Exa RO/S Facilit Facility Facility Facility Comment

m RO y Rec.: Rec.:

Rec Quest Rec.: Two Change

ord ion Delete correct Answer

No. No. / answer

Reaso s

n

129 100/1 No Delete question. No correct answer.

00 Correc Procedure HC.OP-IO.ZZ-0008 was revised to

t remove reference to using HCU Accumulator

Answe pressures as verification means. The

r procedure now uses SPDS, CRIDS or RMCS

Activity Control.

NRC Resolution: Delete the question due to no correct answer.

The NRC requested and reviewed additional material - Documentation of date of procedure

change - 1997. The basis for the change indicates that HCU accumulator pressure is not

adequate as a means of verifying rods are into the core which was the intent of the question.

Based on the above review, NRC staff accepted the facility comment.